Similar Documents at Salem |
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Category:Inservice/Preservice Inspection and Test Report
MONTHYEARLR-N24-0009, In-Service Inspection Activities2024-02-0505 February 2024 In-Service Inspection Activities LR-N23-0054, In-Service Inspection Activities2023-07-26026 July 2023 In-Service Inspection Activities LR-N22-0068, In-Service Inspection Activities - 90-Day Report2022-08-10010 August 2022 In-Service Inspection Activities - 90-Day Report LR-N22-0013, In-Service Inspection Activities - 90-Day Report2022-02-10010 February 2022 In-Service Inspection Activities - 90-Day Report LR-N21-0075, Updated Steam Generator Tube Inspection Report - March 2020 to Reflect TSTF-577 Reporting Requirements2021-11-0202 November 2021 Updated Steam Generator Tube Inspection Report - March 2020 to Reflect TSTF-577 Reporting Requirements LR-N21-0076, Updated Steam Generator Tube Inspection Report - Twenty-second Refueling Outage (2R22) to Reflect TSTF-577 Reporting Requirements2021-11-0101 November 2021 Updated Steam Generator Tube Inspection Report - Twenty-second Refueling Outage (2R22) to Reflect TSTF-577 Reporting Requirements LR-N21-0032, Report of Changes, Tests, and Experiments2021-04-0202 April 2021 Report of Changes, Tests, and Experiments LR-N21-0021, In-Service Inspection Activities - 90-Day Report2021-03-11011 March 2021 In-Service Inspection Activities - 90-Day Report LR-N21-0014, Snubber Program Plan, Fifth Ten-Year Inspection Interval, Effective from January 1, 2021 Through December 31, 20302021-02-16016 February 2021 Snubber Program Plan, Fifth Ten-Year Inspection Interval, Effective from January 1, 2021 Through December 31, 2030 LR-N20-0062, Steam Generator Tube Inspection Report - March 20202020-09-17017 September 2020 Steam Generator Tube Inspection Report - March 2020 LR-N19-0106, Submittal of Program for Salem Units 1 and 2 Fifth Ten-Year Interval Inservice Testing Program2019-11-25025 November 2019 Submittal of Program for Salem Units 1 and 2 Fifth Ten-Year Interval Inservice Testing Program LR-N19-0089, In-Service Inspection Activities - 90-Day Report2019-09-12012 September 2019 In-Service Inspection Activities - 90-Day Report LR-N19-0011, In-Service Inspection Activities - 90-Day Report2019-02-11011 February 2019 In-Service Inspection Activities - 90-Day Report LR-N18-0054, Steam Generator Tube Inspection Report: Twenty-fifth Refueling Outage (1R25)2018-05-0707 May 2018 Steam Generator Tube Inspection Report: Twenty-fifth Refueling Outage (1R25) LR-N17-0174, Steam Generator Tube Inspection Report - Twenty-Second Refueling Outage (2R22)2017-11-21021 November 2017 Steam Generator Tube Inspection Report - Twenty-Second Refueling Outage (2R22) LR-N17-0134, In-Service Inspection Activities, 90-Day Report2017-08-28028 August 2017 In-Service Inspection Activities, 90-Day Report LR-N17-0009, Steam Generator Tube Inspection Report - Twenty-fourth Refueling Outage (1R24)2017-01-20020 January 2017 Steam Generator Tube Inspection Report - Twenty-fourth Refueling Outage (1R24) LR-N16-0187, In-Service Inspection Activities - 90-Day Report, Owner'S Activity Report S1RFO242016-10-11011 October 2016 In-Service Inspection Activities - 90-Day Report, Owner'S Activity Report S1RFO24 LR-N16-0025, In-Service Inspection Activities - 90-Day Report2016-02-26026 February 2016 In-Service Inspection Activities - 90-Day Report LR-N15-0037, In-Service Inspection Activities - 90-Day Report2015-02-23023 February 2015 In-Service Inspection Activities - 90-Day Report LR-N14-0232, Steam Generator Tube - Inspection Report - Twentieth Refueling Outage (2R20)2014-10-30030 October 2014 Steam Generator Tube - Inspection Report - Twentieth Refueling Outage (2R20) ML14070A2542014-03-26026 March 2014 Review of the Fall 2012 Steam Generator Tube Inservice Inspections During Refueling Outage 2R19 LR-N13-0256, Inservice Inspection (Lsi) Program Plan, Fourth Ten-Year Interval2013-11-11011 November 2013 Inservice Inspection (Lsi) Program Plan, Fourth Ten-Year Interval LR-N13-0159, In-Service Inspection Activities - 90-Day Report2013-07-24024 July 2013 In-Service Inspection Activities - 90-Day Report LR-N13-0021, Salem Nuclear Generating Station Unit 2 - Inservice Inspection Activities - 90-Day Report2013-02-0101 February 2013 Salem Nuclear Generating Station Unit 2 - Inservice Inspection Activities - 90-Day Report LR-N13-0021, Inservice Inspection Activities - 90-Day Report2013-02-0101 February 2013 Inservice Inspection Activities - 90-Day Report LR-N11-0382, Inservice Inspection Activities - 90-Day Report2012-01-19019 January 2012 Inservice Inspection Activities - 90-Day Report LR-N11-0213, Inservice Inspection (Lsi) Program Plan, Fourth Ten-Year Interval2011-08-11011 August 2011 Inservice Inspection (Lsi) Program Plan, Fourth Ten-Year Interval LR-N10-0361, Request for Relief from ASME Code Pressure Test for Service Water Supply Buried Piping2010-10-12012 October 2010 Request for Relief from ASME Code Pressure Test for Service Water Supply Buried Piping LR-N10-0256, Submittal of Inservice Inspection Activities - 90-Day Report2010-07-20020 July 2010 Submittal of Inservice Inspection Activities - 90-Day Report LR-N10-0007, Additional Information Related to Relief Requests S1-I3R-93, S2-I3R-94, and SC-I3R-952010-01-13013 January 2010 Additional Information Related to Relief Requests S1-I3R-93, S2-I3R-94, and SC-I3R-95 LR-N10-0002, Inservice Inspection Activities - 90-Day Report2010-01-0808 January 2010 Inservice Inspection Activities - 90-Day Report ML1034404472009-12-23023 December 2009 Document: Inservice Testing Auxiliary Feedwater Valves Mode 3. S2.OP-ST.AF-0007Q Rev. 20 LR-N09-0295, Units 1 and 2, Supplement to License Amendment Request S09-06, Revision to Technical Specification 4.0.5, Surveillance Requirements for Inservice Inspection and Testing of ASME Code Components2009-12-21021 December 2009 Units 1 and 2, Supplement to License Amendment Request S09-06, Revision to Technical Specification 4.0.5, Surveillance Requirements for Inservice Inspection and Testing of ASME Code Components LR-N09-0016, Inservice Inspection Activities - 90-Day Report2009-02-0505 February 2009 Inservice Inspection Activities - 90-Day Report LR-N08-0174, Inservice Inspection Activities - 90-Day Report2008-08-0606 August 2008 Inservice Inspection Activities - 90-Day Report ML0807200682008-02-25025 February 2008 Re-Submittal of Inservice Testing Program Relief Requests P01, V03 and V04 LR-N07-0172, Inservice Inspection Activities - 90-Day Report2007-07-20020 July 2007 Inservice Inspection Activities - 90-Day Report LR-N07-0071, Generation - Unit 2, Withdrawal of Inservice Inspection Program Relief Requests S2-I2-RR-B01 and S2-I2-RR-C012007-03-26026 March 2007 Generation - Unit 2, Withdrawal of Inservice Inspection Program Relief Requests S2-I2-RR-B01 and S2-I2-RR-C01 LR-N07-0045, Steam Generator Tube ISI Summary Report2007-03-0101 March 2007 Steam Generator Tube ISI Summary Report LR-N05-0380, Inservice Inspection Activities - 90 Day Report Fourteenth Refueling Outage Salem Generating Station Unit 22005-08-11011 August 2005 Inservice Inspection Activities - 90 Day Report Fourteenth Refueling Outage Salem Generating Station Unit 2 LR-N05-0240, Inservice Inspection Program Relief Request S2-13-RR-F012005-04-24024 April 2005 Inservice Inspection Program Relief Request S2-13-RR-F01 LR-N05-0168, Relief, Inservice Inspection Program Relief Request S2-13RR-F01 Re Requirements for Testing Dynamic Restraints2005-04-0808 April 2005 Relief, Inservice Inspection Program Relief Request S2-13RR-F01 Re Requirements for Testing Dynamic Restraints LR-N04-0328, Inservice Inspection Activities - 90 Day Report Sixteenth Refueling Outage2004-09-0101 September 2004 Inservice Inspection Activities - 90 Day Report Sixteenth Refueling Outage LR-N04-0299, Inservice Inspection Program Relief Requests S1-RR-04-V01 and V022004-07-0909 July 2004 Inservice Inspection Program Relief Requests S1-RR-04-V01 and V02 ML0408000072004-05-0404 May 2004 Review of Inservice Inspection Reports for Steam Generator Tube Inspections Conducted During the 2002 Refueling Outages LR-N04-0130, Update ASME XI Code of Record, Request That Relief Request S1-I3-RR-A13 Be Withdrawn2004-03-24024 March 2004 Update ASME XI Code of Record, Request That Relief Request S1-I3-RR-A13 Be Withdrawn LR-N04-0242, Unit 2 - Inservice Inspection Program, Long Term Plan, Third Interval, Revision 0, Volume a, Drawing ISI301 Through ISI2462003-11-30030 November 2003 Unit 2 - Inservice Inspection Program, Long Term Plan, Third Interval, Revision 0, Volume a, Drawing ISI301 Through ISI246 LR-N04-0424, Unit 2 - Inservice Inspection Program, Long Term Plan, Third Interval, Revision 0, Volume a, Appendix C Through Appendix E2003-11-30030 November 2003 Unit 2 - Inservice Inspection Program, Long Term Plan, Third Interval, Revision 0, Volume a, Appendix C Through Appendix E LR-N02-0453, Supplemental Information Inservice Inspection Program Relief Requests S2-RR-03-V01 and V022003-10-24024 October 2003 Supplemental Information Inservice Inspection Program Relief Requests S2-RR-03-V01 and V02 2024-02-05
[Table view] Category:Letter type:LR
MONTHYEARLR-N24-0068, Core Operating Limits Report - Cycle 282024-10-21021 October 2024 Core Operating Limits Report - Cycle 28 LR-N24-0063, Emergency Plan Document Revision Implemented September 18, 2024. Includes NC.EP-EP.ZZ-0903, Rev. 7, Opening of Emergency Operations Facility (EOF)2024-10-0707 October 2024 Emergency Plan Document Revision Implemented September 18, 2024. Includes NC.EP-EP.ZZ-0903, Rev. 7, Opening of Emergency Operations Facility (EOF) LR-N24-0012, Application to Revise Technical Specifications and 10 CFR 50.12 Exemption Request to Implement Optimized ZIRLO Fuel Rod Cladding2024-07-24024 July 2024 Application to Revise Technical Specifications and 10 CFR 50.12 Exemption Request to Implement Optimized ZIRLO Fuel Rod Cladding LR-N24-0041, Stations, Revisions to Emergency Plan Document Nc EP-EP-ZZ-01102, Rev. 28, Emergency Coordinator Response2024-05-22022 May 2024 Stations, Revisions to Emergency Plan Document Nc EP-EP-ZZ-01102, Rev. 28, Emergency Coordinator Response LR-N24-0039, Steam Generator Tube Inspection Report - Twenty-ninth Refueling Outage2024-05-0606 May 2024 Steam Generator Tube Inspection Report - Twenty-ninth Refueling Outage LR-N24-0034, 2023 Annual Radioactive Effluent Release Report (ARERR)2024-04-30030 April 2024 2023 Annual Radioactive Effluent Release Report (ARERR) LR-N24-0035, 2023 Annual Radiological Environmental Operating Report (AREOR)2024-04-30030 April 2024 2023 Annual Radiological Environmental Operating Report (AREOR) LR-N24-0024, Response to Request for Additional Information Associated with License Amendment Request (LAR) to Modify the Salem and Hope Creek Exclusion Area Boundary2024-04-26026 April 2024 Response to Request for Additional Information Associated with License Amendment Request (LAR) to Modify the Salem and Hope Creek Exclusion Area Boundary LR-N24-0011, Supplemental Information to License Amendment Request (LAR) to Modify the Salem and Hope Creek Exclusion Area Boundary2024-04-0505 April 2024 Supplemental Information to License Amendment Request (LAR) to Modify the Salem and Hope Creek Exclusion Area Boundary LR-N24-0028, And Salem Generating Station - Notice of Intent to Pursue Subsequent License Renewal2024-03-28028 March 2024 And Salem Generating Station - Notice of Intent to Pursue Subsequent License Renewal LR-N24-0021, And Salem Generating Station, Units 1 and 2 - Guarantees of Payment of Deferred Premiums2024-03-20020 March 2024 And Salem Generating Station, Units 1 and 2 - Guarantees of Payment of Deferred Premiums LR-N24-0020, Generation Station and Salem Generating Station, Units 1 & 2 - Annual Property Insurance Status Report2024-03-0707 March 2024 Generation Station and Salem Generating Station, Units 1 & 2 - Annual Property Insurance Status Report LR-N24-0022, Spent Fuel Cask Registration2024-02-29029 February 2024 Spent Fuel Cask Registration LR-N24-0009, In-Service Inspection Activities2024-02-0505 February 2024 In-Service Inspection Activities LR-N23-0079, Special Report 23-02-00 Pursuant to the Requirements of Salem Unit 1 Technical Specification 3.3.3.7, Action 10, for the Unit 1 Main Steam Line Rad Monitor Inoperable for Greater than Seven Days2023-12-0707 December 2023 Special Report 23-02-00 Pursuant to the Requirements of Salem Unit 1 Technical Specification 3.3.3.7, Action 10, for the Unit 1 Main Steam Line Rad Monitor Inoperable for Greater than Seven Days LR-N23-0077, Loss of Coolant Accident Peak Cladding Temperature Margin Tracking - Annual Report 2023 & 30 Day Report for Salem Unit 1 Upflow Conversion2023-11-29029 November 2023 Loss of Coolant Accident Peak Cladding Temperature Margin Tracking - Annual Report 2023 & 30 Day Report for Salem Unit 1 Upflow Conversion LR-N23-0072, Core Operating Limits Report – Cycle 302023-11-0101 November 2023 Core Operating Limits Report – Cycle 30 LR-N23-0045, And Peach Bottom Atomic Power Station, Units 2 and 3 - Notice of Proposed Amendment to Decommissioning Trust Agreement2023-09-0808 September 2023 And Peach Bottom Atomic Power Station, Units 2 and 3 - Notice of Proposed Amendment to Decommissioning Trust Agreement LR-N23-0055, Special Report 272/23-01-00, Pursuant to the Requirements of Technical Specification 3.3.3.1, Action 23, for the Vent Noble Gas Rad Monitor Inoperable for Greater than Seven Days2023-08-0303 August 2023 Special Report 272/23-01-00, Pursuant to the Requirements of Technical Specification 3.3.3.1, Action 23, for the Vent Noble Gas Rad Monitor Inoperable for Greater than Seven Days LR-N23-0054, In-Service Inspection Activities2023-07-26026 July 2023 In-Service Inspection Activities LR-N23-0046, Emergency Plan Document Revisions Implemented June 28, 20232023-07-10010 July 2023 Emergency Plan Document Revisions Implemented June 28, 2023 LR-N23-0005, License Amendment Request to Amend Technical Specifications (TS) 6.8.4.f for Permanent Extension of Type a and Type C Leak Rate Test Frequencies2023-06-23023 June 2023 License Amendment Request to Amend Technical Specifications (TS) 6.8.4.f for Permanent Extension of Type a and Type C Leak Rate Test Frequencies LR-N23-0035, 2022 Annual Radioactive Effluent Release Report (ARERR)2023-04-27027 April 2023 2022 Annual Radioactive Effluent Release Report (ARERR) LR-N23-0034, 2022 Annual Radiological Environmental Operating Report (AREOR) - Salem Nuclear Generating Station, Unit Nos. 1 and 2 and Hope Creek Generating Station2023-04-27027 April 2023 2022 Annual Radiological Environmental Operating Report (AREOR) - Salem Nuclear Generating Station, Unit Nos. 1 and 2 and Hope Creek Generating Station LR-N23-0033, Core Operating Limits Report – Cycle 272023-04-26026 April 2023 Core Operating Limits Report – Cycle 27 LR-N23-0010, License Amendment Request Revision of Technical Specification (TS) to Delete TS Section 5.5 - Meteorological Tower Location2023-04-21021 April 2023 License Amendment Request Revision of Technical Specification (TS) to Delete TS Section 5.5 - Meteorological Tower Location LR-N23-0006, Report on Status of Decommissioning Funding for Reactors and Independent Spent Fuel Storage Installations2023-03-24024 March 2023 Report on Status of Decommissioning Funding for Reactors and Independent Spent Fuel Storage Installations LR-N23-0019, And Salem Generating Station, Units 1 and 2 - Guarantees of Payment of Deferred Premiums2023-03-21021 March 2023 And Salem Generating Station, Units 1 and 2 - Guarantees of Payment of Deferred Premiums LR-N23-0016, And Salem Generating Station, Units 1 and 2 - Report of Changes, Tests, and Experiments2023-02-28028 February 2023 And Salem Generating Station, Units 1 and 2 - Report of Changes, Tests, and Experiments LR-N23-0012, Annual Property Insurance Status Report2023-02-24024 February 2023 Annual Property Insurance Status Report LR-N23-0014, Stations Submittal of 2022 Annual Report of Fitness for Duty Performance Data Per 10 CFR 26.203(e) and 10 CFR 26.7172023-02-23023 February 2023 Stations Submittal of 2022 Annual Report of Fitness for Duty Performance Data Per 10 CFR 26.203(e) and 10 CFR 26.717 LR-N23-0003, Response to Requests for Additional Information Salem Unit 2 Relief Request S2-I4R-2112023-02-0101 February 2023 Response to Requests for Additional Information Salem Unit 2 Relief Request S2-I4R-211 LR-N22-0096, And Salem Generating Station, Units 1 and 2 - Request for Threshold Determination2023-01-0505 January 2023 And Salem Generating Station, Units 1 and 2 - Request for Threshold Determination LR-N22-0095, Loss of Coolant Accident Peak Cladding Temperature Margin Tracking - Annual Report 20222022-12-20020 December 2022 Loss of Coolant Accident Peak Cladding Temperature Margin Tracking - Annual Report 2022 LR-N22-0094, Emergency Plan Document Revisions Implemented November 21, 20222022-12-14014 December 2022 Emergency Plan Document Revisions Implemented November 21, 2022 LR-N22-0092, Response to Final Iolb Request for Additional Information for Salem LAR to Revise TS to Extend Allowed Outage Time for Inoperable EDG2022-12-0909 December 2022 Response to Final Iolb Request for Additional Information for Salem LAR to Revise TS to Extend Allowed Outage Time for Inoperable EDG LR-N22-0091, Independent Spent Fuel Storage Installation, Report of 10 CFR 72.48 Changes, Tests, and Experiments2022-12-0202 December 2022 Independent Spent Fuel Storage Installation, Report of 10 CFR 72.48 Changes, Tests, and Experiments LR-N22-0084, Response to Final Request for Additional Information for Salem LAR to Revise TS to Extend Allowed Outage Time for Inoperable EDG (EPID L- 2022-LLA-0095)2022-11-17017 November 2022 Response to Final Request for Additional Information for Salem LAR to Revise TS to Extend Allowed Outage Time for Inoperable EDG (EPID L- 2022-LLA-0095) LR-N22-0090, Supplement to Submittal of Salem Generating Station Updated FSAR, Revision 33, 10 CFR 71.106 Review Results and 10 CFR 54.37(b) Review Results for Salem2022-11-10010 November 2022 Supplement to Submittal of Salem Generating Station Updated FSAR, Revision 33, 10 CFR 71.106 Review Results and 10 CFR 54.37(b) Review Results for Salem LR-N22-0065, Submittal of Relief Request Associated with the Fourth Inservice Inspection (ISI) Interval Limited Examinations2022-09-27027 September 2022 Submittal of Relief Request Associated with the Fourth Inservice Inspection (ISI) Interval Limited Examinations LR-N22-0074, Emergency Plan Evacuation Time Estimate2022-09-15015 September 2022 Emergency Plan Evacuation Time Estimate LR-N22-0066, License Amendment Request (LAR) to Relocate Technical Specifications (TS) Requirements for Reactor Head Vents to the Technical Requirements Manual (TRM)2022-08-31031 August 2022 License Amendment Request (LAR) to Relocate Technical Specifications (TS) Requirements for Reactor Head Vents to the Technical Requirements Manual (TRM) LR-N22-0063, Spent Fuel Cask Registration2022-08-10010 August 2022 Spent Fuel Cask Registration LR-N22-0068, In-Service Inspection Activities - 90-Day Report2022-08-10010 August 2022 In-Service Inspection Activities - 90-Day Report LR-N22-0012, License Amendment Request to Amend the Technical Specifications to Revise and Relocate the Reactor Coolant System Pressure and Temperature Limits and Pressurizer Overpressure Protection System Limits to a Pressure and Temperature2022-08-0707 August 2022 License Amendment Request to Amend the Technical Specifications to Revise and Relocate the Reactor Coolant System Pressure and Temperature Limits and Pressurizer Overpressure Protection System Limits to a Pressure and Temperature LR-N22-0062, Spent Fuel Cask Registration2022-07-21021 July 2022 Spent Fuel Cask Registration LR-N22-0006, License Amendment Request (LAR) to Amend Salem Unit 1 and Unit 2 Technical Specifications (TS) to Extend the Allowed Outage Time for an Inoperable Emergency Diesel Generator from 72 Hours to 14 Days2022-06-29029 June 2022 License Amendment Request (LAR) to Amend Salem Unit 1 and Unit 2 Technical Specifications (TS) to Extend the Allowed Outage Time for an Inoperable Emergency Diesel Generator from 72 Hours to 14 Days LR-N22-0051, License Amendment Request to Relocate Technical Specification Facility/Unit Staff Qualification Requirements to Quality Assurance Topical Report2022-06-22022 June 2022 License Amendment Request to Relocate Technical Specification Facility/Unit Staff Qualification Requirements to Quality Assurance Topical Report LR-N22-0044, Emergency Plan Document Revisions Implemented November, 20212022-05-19019 May 2022 Emergency Plan Document Revisions Implemented November, 2021 LR-N22-0043, Core Operating Limits Report - Cycle 292022-05-0909 May 2022 Core Operating Limits Report - Cycle 29 2024-07-24
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PSEG Nuclear LLC P.O. Box 236, Hancocks Bridge, NJ 08038-0236 0PSEG NudmrLLC ASME Code Case N-532-4 FEB i S Z015 LR-N15-0037 U.S. Nuclear Regulatory Commission AT+N: Document Control Desk Washington, DC 20555-001 Salem Nuclear Generating Station Unit 1 Renewed Facility Operating License DPR-70 NRC Docket No. 50-272
Subject:
In-Service Inspection Activities Day Report This letter submits the Owner's Activity Report for In-Service Inspection (ISi) activities conducted at the Salem Generating Station Unit 1 during the twenty-third refueling outage. This report is submitted in accordance with Code Case N-532-4 "Repair/Replacement Activity Documentation Requirements and In-Service Summary Report Preparation and Submission Section XI, Division 1," and within its ninety (90) day reporting requirement. to this letter contains the required Salem Unit 1 Owner's Activity Report.
There are no commitments contained in this letter.
Should you have any questions regarding this submittal, please contact David Lafleur at (856) 339-1754.
Sincerely, cj'trt:? ;:;-R_
John Perry Site Vice President -
Enclosures (1)
FEB 2 8 2015 Document Control Desk Page 2 LR-N15-0037 cc: Mr. D. Dorman, Administrator, Region I, NRC Ms. C. Sanders, Project Manager, NRC Mr. P. Finney, NRC Senior Resident Inspector, Salem Mr. P. Mulligan, Manager IV, NJBNE Mr. L. Marabella, Corporate Commitment Tracking Coordinator Mr. T. Cachaza, Salem Commitment Tracking Coordinator Mr. Milton Washington, Chief Inspector - Occupational Safety and Health Bureau of Boiler and Pressure Vessel Compliance
Document Control Desk LR-N15-0037 Salem Unit 1 Owners Activity Report - 51 RF023 In Accordance With ASME Section XI Code Case N-532-4
FORM OAR-1 OWNER'S ACTIVITY REPORT S1RF023 Report Number S1RF023 Owner PSEG Nuclear LLC, One Alloway Creek Neck Road, Hancocks Bridge, New Jersey 08038 Plant Salem Generating Station Unit No. 1 Commercial Service Date July 1, 1977 Refueling Outage No. 23 Current Inspection Interval ISi - Fourth (4th) {CISI - Second (2nd)}
Current Inspection Period ISi - Second (2nd) {CISI - Second (2nd)}
Edition and Addenda of Section XI Applicable to the inspection plan ISi and CISI - 2004 Edition Date and revision of inspection plan ISi - July 2012, Revision 1 {CISI - October 2010, Revision O}
Code Cases used N-460, N-532-4, N-566-2, N-706-1 & N-722-1 CERTIFICATE OF CONFORMANCE I certify that (a) the statements made in this report are correct; (b) the examinations and tests meet the Inspection Plan as required by the ASME Code,Section XI; and (c) the repair/replacement activities and evaluations supportin the completion of S1RF023 conform to the requirements of Section XL Signed Edle T. Giles I ISi Pro ram Mana er Date CERTIFICATE OF INSERVICE INSPECTION I, the undersigned, holding a valid commission issued by the National Board of Boiler and Pressure Vessel Inspectors and the State or Province of New Jersey and employed by HSB Global Standards of Connecticut have inspected the items described in this Owner's Activity Report, during the period May 28, 2013 to November 23, 2014, and state that, to the best of my knowledge and belief, the Owner has performed all activities represented by this report in accordance with the requirements of Section XI.
By signing this certificate neither the Inspector nor his employer makes any warranty, expressed or implied, concerning the repair/replacement activities and evaluation described in this report.
Furthermore, neither the Inspector nor his employer shall be liable in any manner for any ersonl injuryJYP erty damage or a loss of any kind arising from or connected with this mspect10n.
David Sherer Commissions NB 10562 A,N,I TN 4161 Inspector's Signature National Board, State, Province, and Endorsements
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FORM OAR-1 OWNER'S ACTIVITY REPORT S1RF023 TABLE 1 ITEMS WITH FLAWS OR RELEVANT CONDITIONS THAT REQUIRED EVALUATION FOR CONTINUED SERVICE Exam Item Item Description Evaluation Description Category Number cc Ll.10 Containment Exterior ASME Section XI Subsection IWL Engineering Concrete Surface Evaluation of exposed reinforcement and loss of concrete cover, found acceptable for continued service and repair scheduled. Evaluation documented in order 70170446.
TABLE2 ABSTRACT OF REPAIR/REPLACEMENT ACTITIES REQUIRED FOR CONTINUED SERVICE Code Item Description Description of Work Date Repair/
Class Completed R eplacement Plan Number Corrosion of steel bell rings in Joints 6, 9 and 42; cleaned, performed UT 24" No. 12 SW Return thickness measurements, coated area 11/14/2014 60111305 Header Buried PCCP Piping, and installed Structural WEKO Seal, 3 Inside Joints 6, 9 and 42 Relief Request SC-I4R-133 used.
Coating found degraded allowing inside surface of carbon steel pipe spool corrosion. Perform UT thickness 11/12/2014 60113765 24" No. 12 SW Supply measurement and performed weld build Header Buried Carbon Steel up in 3 areas below minimum wall, 3 Piping Spool No. l-SW-67 recoated entire area.
No. 13 Charging Pump Cylinder No. 4 No. 13 Charging Pump, leak. Replaced Charging Pump Cylinder 08/18/2014 60117715 2 (1CVE22) Head Assemblv.
MSG-111 Integral Attachment Weld Main Steam Pipe Support indication found during ISI 11/12/2014 60119897 MSG-111 Integral examination, removed flaw and weld 2 Attachment Weld repaired 1/4" Capillary Tubing on 1/4" Capillary tube leak on line to lPA2405 Containment Wide lPA2405, leaking tubing replaced. 11/27/2014 60120134 1 Range Pressure Channel IV 1/4" Capillary Tubing to 1/4" Capillary tubing on line 6522-XD lLL3614ZlB RPV Level weld leak, replaced weld and capillary 11/24/2014 60120197 Head Hydraulic Sensor tubing.
2 Bellow 1/4" Capillary RVLIS Sensing Line 1/4" RVLIS Sensing Line to 6528-XB tube leak, Cut and capped 01/09/2015 60120462 1 1LT1312 tubing at leak location 3/8" Tubing down stream of 3/8" Tubing leak at valve 11 SW226, 03/27/2014 60114348 3 isolation valve 11 SW226 replaced tubing.
Leak in 3/4" piping to valve butt weld at 3/4" Piping to isolation valve inlet side of valve 13SW10, replaced 03/10/2014 60115349 3 13SW10 valve and piping.
2" Screen Wash Valve 2" 14SW15 valve body through wall 07/10/2013 60111688 3 14SW15 leak, replaced valve.
3/8" Tubing down stream of 3/8" Tubing leak at valve 15SW226, 03/18/2014 60114346 3 isolation valve 15SW226 replaced tubing.
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FORM OAR-1 OWNER'S ACTIVITY REPORT S1RF023 Valve 12RH10 gasket leakage and 8" RHR Pump Discharge bonnet bolting corrosion (boric acid), 12/04/2014 60119726 2 Stop Valve 12RH10 replaced gasket and bolting.
Examination of Containment Liner Test Channels underneath insulation system identified corrosion of test channels.
Removed degraded liner test channels, 11/19/2014 60113828 Containment Liner Test performed UT Thickness measurements Channels underneath of liner, restored liner coatings and insulation system (License sealed test channels to prevent moisture MC Renewal Examination) intrusion.
Examination of Containment Liner underneath insulation system identified degraded coatings. Cleaned Containment Liner Containment Liner, performed UT 11/19/2014 60113828 underneath insulation system thickness measurements (No significant (License Renewal wall loss identified) and repaired MC Examination) coatings.
During Section XI examination support 1C-12SWH-9 Variable Spring Can Hanger setting found out of tolerance.
11112/2014 70170986 Additional supports examined and 1C-12SWH-9 Variable support 1C-12SWH-9 adjusted with in 3 Soring Can Hanger tolerance.
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