LR-N10-0256, Submittal of Inservice Inspection Activities - 90-Day Report

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Submittal of Inservice Inspection Activities - 90-Day Report
ML102150075
Person / Time
Site: Salem PSEG icon.png
Issue date: 07/20/2010
From: Fricker C
Public Service Enterprise Group
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
LR-N10-0256
Download: ML102150075 (5)


Text

PSEG Nuclear LLC `

P.O. Box 236, Hancocks Bridge, New Jersey 08038-0236 JUL 2 O'2D1O 0 PSEG NuclearLLC LR-N 10-0256 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington DC 20555-001 Salem Nuclear Generating Station Unit 1 Facility Operating License No. DPR-70 NRC Docket No. 50-272

SUBJECT:

Inservice Inspection Activities Day Report This letter submits the Owner's Activity Report for Inservice Inspection (ISI) activities conducted at the Salem Generating Station Unit No. 1 during the twentieth refueling outage. This report is submitted in accordance with Code Case N-532-4 "Repair /

Replacement Activity Documentation Requirements and Inservice Summary Report Preparation and Submission Section Xl, Division 1," and within the ninety (90) day reporting requirement.

Enclosure 1 to this letter contains the required Salem Unit I Owner's Activity Report.

There are no commitments contained in this letter.

Should you have any questions regarding this submittal, please contact E. H. Villar at (856) 339-5456.

Sincer arI .ricker Site Vice President.- Salem Enclosures (1)

AI0J7 95-2168 REV. 7/99

Nuclear Regulatory Commission Jtjj , 2010 Page 2 LR-N10-0256 cc Mr. W. Dean, Administrator - Region I Mr. R. Ennis, Licensing Project Manager - Salem USNRC Senior Resident Inspector - Salem (X24)

Mr. P. Mulligan, Manager IV Mr. H. Berrick, Salem Commitment Tracking Coordinator Mr. L. Marabella, Corporate Commitment Tracking Coordinator Mr. Milton Washington Chief Inspector NJ Department of Labor Division of Public Safety, Occupational Safety and Health Bureau of Boiler and Pressure Vessel Compliance P. O. Box 396 101 South Broad Street Trenton, NJ 08625-0392

Nuclear Regulatory Commission LR-N10-0256 Salem Unit 1 Owner's Activity Report - S1 R20 In Accordance With ASME Section XI Code Case N-532-4

FORM OAR-1 OWNER'S ACTIVITY REPORT Report Number S1RF020 Owner PSEG Nuclear LLC, PO. Box 236, Hancocks Bridge, NJ 08038 Plant Salem Generating Station Unit No. 1 Commercial Service Date July 1, 1977. Refueling Outage No. 20 Current Inspection Interval ISI - Third (3 r) {Containment IWE/IWL First (lst)}.

Current Inspection Period ISI - Third ( 3 r) {Containment IWE/IWL Third ( 3 rd)}

Edition and Addenda of Section XI Applicable to the inspection plan; ISI - 1998 Edition - 2000 Addenda;. Containment IWE/IWL -w1998 Edition -1998 Addenda Date and revision of inspection plan March 2009, Revision 2 Edition & Addenda of Section XI Applicable to repairs and replacements, if different than the inspection plan (Unless specifically. identified in the individual repair plan)

ASME Class 1, 2 and 3-41998 Edition, 2000 Addenda; Class MC - 1992 Edition, 1992 Addenda CERTIFICATE OF CONFORMANCE I certify. that the statements made in this report are correct; (b) the examinations and tests meet the Inspection Plan as required by the ASME Code,Section XI; and (c) the repair/replacement activities and evaluations supporting the completion of SIRFO20. conform to the requirements of Section XI.

Signed * ....... Edley T. Giles /ISI Program Manager 5 Z// 0 Owner or Owner's Designee, Title Date CERTIFICATE OF INSERVICE INSPECTION I, the undersigned, holding a valid commission issued by the National Board of Boiler and Pressure Vessel Inspectors and the State or Province of New York and employed by Hartford Steam Boiler Inspection and Insurance Company of Connecticut have inspected the items described in this Owner's Activity Report, during the period November 15, 2008 to April 29, 2010, and state that, to the best of my knowledge and belief, the Owner has performed all activities represented by this report in accordance with the requirements of Section XI.

By signing this certificate neither the Inspector nor his employer makes any warranty, expressed or implied, concerning the repair/replacement activities and evaluation described in this report.

Furthermore, neither the Inspector nor his employer shall be liable in any manner for any personal injury or property damage or a loss of any kind arising from or connected with this inspection.

W/Wy,14,z Commissions I/1 f ýe A I

Inspector'signattu National Board, State, Province, and Endorsements Date 1-/3/7-0/.0

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FORM OAR-1 OWNER'S ACTIVITY REPORT TABLE 1 ITEMS WITH FLAWS OR RELEVANT CONDITIONS THAT REQUIRED EVALUATION FOR CONTINUED SERVICE Exam Item Item Description Evaluation Description Category Number N/A N/A None N/A TABLE 2 ABSTRACT OF REPAIR/REPLACEMENT ACTIVITIES REQUIRED FOR CONTINUED SERVICE Code Item Description Description of Work Date Repair/

Class Completed Replacement Plan Number Clean, Perform UT Thickness Examination and Restore Coating and Containment Liner Corrosion Moisture Barrier on Containment Liner 05/04/2010 60086175 at 78' between floor and at 78' between floor and Leak Test MC Leak Test Channel Channel 3/4" Valve 11 SW64 Leaking 11 SW64 was cut out and replaced with 16 DPM during System 3/4" AL6XN ball valve 11/20/2008 3 Pressure Test SI Room Cooler SW Tubing Replaced 3/8" Tubing and Fittings D/S Leak D/S of 3/8" Valve of 3/8" Valve 1SW179 04/01/2009 60082359 3 1SW179 22 CS Room Cooler- 1.5" Replaced 1.5" Pipe Spool to CS Room 05/19/2009 60083349 3 Piping Leak at Cooler Flange Cooler Flange 12 CVC Pump Room Cooler Replaced 3/8" Valve 1SW651 and U/S Pressure Tap 3/8" Valve tubing. 07/09/2009 60084466 3 1SW651 tubing leak.

11 Chiller condenser recirc Replaced entire spool D/S of Valve pump discharge pressure 11 SW225 gage, Leak D/S of 3/4" 10/09/2009 60086109 Valve 1 1SW225 on pipe reducer connection to 3 instrument tubing Leak in Elbow D/S of 3/4" Replaced Piping and Elbow D/S of 3/4" 10/29/2009 60086502 3 Valve 14SW243 Valve 14SW243 Leak in Piping D/S of 3/4" Replaced D/S Piping and 3/4" Valve 04/06/2010 60083758 3 Valve 11 SW243 II SW243 Component Cooling Leak on Replaced 3/4" Piping to Valve CC221 01/14/2010 60088036 3 Piping to 3/4" Valve CC221 12 CC HX Leak on weld to Replaced 3/4" Valve 12SW398 and Pipe 1/14/2010 60087475 3 3/4" Valve 12SW398 Nipple Leak in Piping D/S of 3/4" Replaced 3/4" Valve 14SW243 and Valve 14SW243 Additional Piping 10/02/2009 60084833 3 Leak not in Order 60086502 4" Auxiliary Feedwater Replaced Entire Portion of Buried 60089561 Buried Piping to SG - Auxiliary Feedwater 4" Piping 04/30/2010 60089848 3 External Wall Loss

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