LR-N10-0002, Inservice Inspection Activities - 90-Day Report

From kanterella
Jump to navigation Jump to search
Inservice Inspection Activities - 90-Day Report
ML100260566
Person / Time
Site: Salem PSEG icon.png
Issue date: 01/08/2010
From: Fricker C
Public Service Enterprise Group
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
LR-N10-0002
Download: ML100260566 (5)


Text

y PSEG Nuclear LLC P.O. Box 236, Hancocks Bridge, NJ 08038-0236

@PonEG NuclearLLC January 8, 2010 LR-N 10-0002 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, DC 20555-001 Salem Nuclear Generating Station Unit 2 Facility Operating License No. DPR-75 NRC Docket No. 50-311

Subject:

Inservice Inspection Activities Day Report This letter submits the Owner's Activity Report for Inservice Inspection (ISI) activities conducted at the Salem Generating Station Unit 2 during the seventeenth refueling outage. This report is submitted in accordance with Code Case N-532-4 "Alternative Requirements to Repair and Replacement Documentation Requirements and Inservice Summary Report Preparation and Submission Section Xl, Division 1," and within its ninety (90) day reporting requirement.

Enclosure 1 to this letter contains the required Salem Unit 2 Owner's Activity Report.

There are no commitments contained in this letter.

Should you have any questions regarding this submittal, please contact E. H. Villar at (856) 339-5456.

Sinceiy

/Car J. ricker Site Vice President - Salem Enclosures (1) vA

,4,

I 4 Document Control Desk January 8, 2010 Page 2 LR-N10-0002 C Mr. S. Collins, Administrator - Region I Mr. R. Ennis, Project Manager -Salem USNRC Senior Resident Inspector - Salem (X24)

Mr. P. Mulligan, Manager IV Commitment Coordinator Salem PSEG Corporate Commitment Manager Mr. Milton Washington, Chief Inspector

Document Control Desk January 8, 2010 LR-N 10-0002 Salem Unit 2 Owners Activity Report - S2R1 7 In Accordance With ASME Section XI Code Case N-532- 4

FORM OAR-1 OWNER'S ACTIVITY REPORT Report Number S2RFO17 Owner PSEG Nuclear LLC, PO Box 236, Hancocks Bridge, NJ 08038 Plant Salem Generating Station Unit No. 2 Commercial Service Date Oct. 31,1981 Refueling Outage No. 17 Current Inspection Interval ISI - Third (3 rd) {Containment IWE/IWL First (lst)}

Current Inspection Period ISI - Second (2 nd) {Containment IWE/IWL Third ( 3 rd)}

Edition and Addenda of Section XI Applicable to the inspection plan; ISI - 1998 Edition - 2000 Addenda; Containment IWE/IWL - 1998 Edition -1998 Addenda Date and revision of inspection plan March 2009, Revision 1 Edition & Addenda of Section XI Applicable to repairs and replacements, if different than the inspection plan (Unless specifically identified in the individual repair plan)

ASME Class 1, 2 and 3 - 1998 Edition, 2000 Addenda; Class MC - 1992 Edition, 1992 Addenda CERTIFICATE OF CONFORMANCE I certify that the statements made in this report are correct; (b) the examinations and tests meet the Inspection Plan as required by the ASME Code,Section XI; and (c) the repair/replacement activities and evaluations supporting the completion of S2RFO 17 conform to the requirements of Section XI.

Signed Edley T. Giles 1.ISI Program Manager 01/05/2010 Owner's Designee, Title Date CERTIFICATE OF INSERVICE INSPECTION I, the undersigned, holding a valid commission issued by the National Board of Boiler and Pressure Vessel Inspectors and the State or Province of New Jersey and employed by Hartford Steam Boiler Inspection and Insurance Company of Connecticut have inspected the items described in this Owner's Activity Report, during the period May 09, 2008 to November 11, 2009, and state that, to the best of my knowledge and belief, the Owner has performed all activities represented by this report in accordance with the requirements of Section XI.

By signing this certificate neither the Inspector nor his employer makes any warranty, expressed or implied, concerning the repair/replacement activities and evaluation described in this report.

Furthermore, neither the Inspector nor his employer shall be liable in any manner for any personal injury or property damage or a loss of any kind arising from or connected with -this inspection.

Commissions ,trcg

\. Inspector's Signature National Board, State, Province, and Endorsements Date '/c72,/e;?5i*5 FORM OAR-I OWNER'S ACTIVITY REPORT TABLE 1 ITEMS WITH FLAWS OR RELEVANT CONDITIONS THAT REQUIRED EVALUATION FOR CONTINUED SERVICE Exam Item Item Description Evaluation Description Category Number E-A El.11 Containment Liner Corrosion at 78' between floor and Technical Input to Operability Leak Test Channel Evaluation (09-021 )of Potential Containment Liner Corrosion DRN 0108-0373-01 (PSEG Nuclear VTD 901897, Sheet 1)

Revision 0 TABLE 2 ABSTRACT OF REPAIR/REPLACEMENT ACTITIES REQUIRED FOR CONTINUED SERVICE Code Item Description Description of Work Date Repair/

Class Completed Replacement Plan Number Hanger S2RHR- Replaced Pipe Hanger 2-RHRH- 05/30/2008 60075919 2 2RHRH21-16 Corroded 21-16 CCW Piping Leak U/S Replaced S2CC -2CC183 and of Valve S2CC - U/S Piping 04/23/2008 60076062 2 2CC183 Piping Corrosion U/S of Replaced Valve S2CC -2CC1 80 Valve S2CC -2CC180 and U/S Piping, Repaired 06/12/2008 60076064 2 Penetration Hanger 2C-24-SIG-518 Hanger 2C-24-SIG-518 Repaired 07/24/2008 60076234 1 Missing Stud Tubing Leak near Replaced Tubing and fitting at 04/22/2008 60076364 3 S2SW -2SW449 S2SW -2SW449 Tubing Leak D/S of Replaced Tubing D/S of Valve 10/31/2009 60076705 2 Valve S2SS -2SS110 S2SS-2SS110 Leak D/S of Valve Replaced Tubing and Fittings 06/02/2008 60077045 3 S2SW -2SW340 D/S of Valve S2SW -2SW340 Leak in tubing D/S of Replaced tubing D/S of Valve 10/04/2008 60078450 2 Valve S1 CVC-1 CV299 S1 CVC -1 CV299 Leak D/S of Valve Replaced Flange and Tubing 02/04/2009 60081138 3 S2SW -21 SW97 D/S of Valve S2SW -21 SW97 Leak at flange to 22 Replaced Flange and Nozzle to Containment Spray S2SW -2SWE22 Room Cooler 07/14/2009 60083349 Pump Room Cooler 3 S2SW -2SWE22