IR 05000277/2005302

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IR 05000352-05-302, 05000353-05-302, 05000277-05-302 and 05000278-05-302; June 13-15, 2005; Limerickand Peach Bottom Stations; Initial Limited Senior Operator Licensing (Lsro) Examination. Three of Three Applicants Passed the Examinations
ML052160317
Person / Time
Site: Peach Bottom, Limerick  Constellation icon.png
Issue date: 08/04/2005
From: Conte R
Division of Reactor Safety I
To: Crane C
Exelon Generation Co, Exelon Nuclear
Shared Package
ML042440144 List:
References
IR-05-302
Download: ML052160317 (34)


Text

August 4, 2005 Mr. Christopher President and CNO Exelon Nuclear Exelon Generation Company, LLC 200 Exelon Way KSA 3-E Kennett Square, PA 19348 SUBJECT: LIMERICK GENERATING STATION UNIT 1 AND UNIT 2 AND PEACH BOTTOM ATOMIC POWER STATION UNIT 2 AND UNIT 3 LIMITED SENIOR REACTOR OPERATOR INITIAL EXAMINATION REPORT NOS. 05000352/2005302, 0500353/2005302, 05000277/2005302 AND 05000278/2005302

Dear Mr. Crane:

This report transmits the results of the Limited Senior Reactor Operator (LSRO) licensing examinations conducted by the NRC during the period of June 13-15, 2005. The examinations addressed areas important to public health and safety and were developed and administered using the guidelines of the Examination Standards for Power Reactors (NUREG-1021, Revision 9).

Based on the results of the examination, all three applicants passed all portions of the examination. The applicants included three LSROs. Examination results indicated that the applicants were well prepared for the examination. Mr. J. Caruso, Chief Examiner, discussed performance insights observed during the examination with Mr. C. Rich on June 15, 2005. On July 21, 2005, final examination results were given during a telephone call between Mr.

J. Caruso and Mr. C. Rich of your training organization. The issuance of license numbers will be delayed pending receipt of written certification from Exelon to the U.S. Nuclear Regulatory Commission stating that the applicants have acquired all experience for which they were previously granted waivers.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRCs document system (ADAMS). These records include the final examination and are available in ADAMS (Master File - Accession Number ML042440215; LSRO Written - Accession Number ML052060104; LSRO Operating Sections A and B- Accession Number ML0052060114. Note for LSRO examinations there is no Operating Section C. ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Mr. Christopher Should you have any questions regarding this examination, please contact me at (610) 337-5183, or by E-mail at RJC@NRC.GOV.

Sincerely,

/RA Richard J. Conte, Chief Operations Branch Division of Reactor Safety Docket Nos. 50-352, 50-353, 50-277, 50-278 License Nos. NPF-39, NPF-85, DPR-44, DPR-56 Enclosure: Initial Examination Report Nos. 05000352/2005302, 05000353/2005302, 05000277/2005302 and 05000278/2005302 cc w/encl:

Chief Operating Officer, Exelon Generation Company, LLC Site Vice President, Peach Bottom Atomic Power Station Plant Manager, Peach Bottom Atomic Power Station Regulatory Assurance Manager - Peach Bottom Senior Vice President, Mid-Atlantic Operations Vice President - Operations Support Vice President - Licensing and Regulatory Affairs Director, Licensing and Regulatory Affairs, Exelon Generation Company, LLC Vice-President, General Counsel and Secretary J. Bradley Fewell, Assistant General Counsel, Exelon Nuclear D. Quinlan, Manager, Financial Control, PSEG R. McLean, Power Plant and Environmental Review Division (MD)

Director, Nuclear Training, Peach Bottom Manager, Operations Training, Peach Bottom Correspondence Control Desk Site Vice President - Limerick Generating Station Plant Manager, Limerick Generating Station Regulatory Assurance Manager, Limerick Senior Vice President - Nuclear Services Vice President - Mid-Atlantic Operations Manager, Licensing - Limerick Generating Station Director, Training, Limerick Generating Station Chairman, Board of Supervisors of Limerick Township D. Allard, Director, Pennsylvania Bureau of Radiation Protection (SLO, PA)

Commonwealth of Pennsylvania (c/o R. Janati, Chief, Division of Nuclear Safety, Pennsylvania Bureau of Radiation Protection)

R. Fletcher, Maryland Department of Environment T. Snyder, Director, Air and Radiation Management Administration, Maryland Department of the Environment (SLO, MD)

Mr. Christopher

SUMMARY OF FINDINGS

IR 05000352/2005302, 05000353/2005302, 05000277/2005302 and 05000278/2005302;

June 13-15, 2005; Limerick Generating Station and Peach Bottom Atomic Power Station; Initial Limited Senior Operator Licensing (LSRO) Examination. Three of three applicants passed the examination (3 LSROs).

The written examinations were administered by the facility and the operating tests were administered by 2 NRC region-based examiners. There were no inspection findings of significance associated with the examinations.

A. Inspector Identified Findings No findings of significance were identified.

B. Licensee Identified Findings No findings of significance were identified.

ii

REPORT DETAILS

REACTOR SAFETY

Mitigating Systems - Limited Senior Reactor Operator (LSRO) Initial License Examination

a. Scope

of Review The facility developed the written and operating initial examination and together with NRC Region I examiner staff verified or ensured, as applicable, the following:

  • The examination was prepared and developed in accordance with the guidelines of Revision 9 of NUREG-1021, "Operator Licensing Examination Standards for Power Reactors. A review was conducted both in the Region I office and at the Limerick plant and training facility. Final resolution of comments and incorporation of test revisions were conducted during and following the onsite preparation week.
  • A test item analysis was completed on the written examination for feedback into the systems approach to training program.
  • Examination security requirements were met.

The NRC examiners administered the operating portion of the examination to all applicants from June 13-14, 2005. Limerick training staff administered the written examination on June 15, 2005.

b. Findings

Grading and Results Three of three applicants (3 LSROs) passed all portions of the initial licensing examination.

The facility had two post-examination comments. These are detailed in Attachment 2.

One procedure enhancement issue was identified during the administration of the Operating Test at Limerick. This was communicated to the licensee.

Examination Administration and Performance No findings of significance were identified.

4OA6 Exit Meeting Summary

On July 21, 2005, the NRC provided conclusions and examination results to a Limerick management representative via the telephone. License numbers for the applicants were not provided at this time pending receipt of written certification from Exelon to the U.S. Nuclear Regulatory Commission stating that the applicants have acquired all experience for which they were previously granted waivers. The NRC expressed appreciation for the cooperation and assistance provided by the licensees training staff during the preparation and administration of the examination.

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

J. White, Director of Training
C. Rich, Manager, Operator Training
C. Fritz, Facility Exam Development Team
C. Goff, Facility Exam Development Team

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

ITEM NUMBER TYPE DESCRIPTION

NONE

ATTACHMENT 2

Licensees Post Written Examination Comments Publically Available

ADAMS Accession No. ML052060249

The licensees post exam comments regarding Questions 26 and 37 were received by the NRC

on June 17, 2005. After initial review, the NRC provided comments to and requested additional

information from the licensee on June 20, 2005. After further review by the NRC staff and

discussions with the licensee, the licensee submitted revised comments for both LSRO

questions #26 and #37, dated and received in Region I on June 22, 2005 (see below). The

NRC provided the licensee further comments on July 5, 2005 regarding question #37 and

certain stated assumptions made by the applicants and the fact that under the conditions stated

in the stem that there was no technical basis for assuming that Fuel Pool Cleanup was either

NOT running at the onset, nor for assuming it was lost following the event. The licensee

submitted a third and final revision for question #37 on July 11, 2005. During the exam there

were no questions from the applicants regarding either LSRO question #26 or #37. The NRCs

resolution for these two post exam comments is based on the independent reviews that were

conducted by both NRC examiners assigned to the exam team (plus a third independent

examiner for the final submittal on question #37) as well as the Branch Chief. There was some

additional input from a DRP Engineer who was a former Peach Bottom SRO.

Original LSRO Question 37:

PBAPS Unit 2 plant conditions are as follows:

- Mode 5

- Core Shuffle Part 1 has just begun

- RBCCW is backing up TBCCW

- The CRD system is in service

- The RWCU system is in service in a normal lineup dumping 60 GPM to the Main

Condenser

- A fire header break in the RBCCW system room has caused both RBCCW

pumps to trip

WHICH ONE of the following describes the operational implications of this condition?

A. Higher than normal plant dose rates.

B. Loss of Instrument Air to the Refueling Bridge

C. Reactor Cavity and fuel pool visibility will degrade

D. Reactor Cavity and Fuel Pool water level will begin to lower.

Originally designated correct answer D Submitted answer explanation (original):

Justification

a. Incorrect - RWCU will not isolate on high temperature. The isolation temperature is

200 degrees F but the Reactor Cavity temperature will be between 110 F and 130 F

during refueling operations. Generally, the temperature is maintained well below 110 F;

around 90 F.

b. Incorrect - The Refueling Bridge at PBAPS has an air compressor mounted on the

bridge and is, therefore, independent of station air systems.

c. Incorrect- RWCU will not isolate on high temperature. The clarity of the Reactor Cavity

will not change due to this event.

d. Correct- With RBCCW supplying TBCCW loads, RBCCW is supplying cooling water to

the CRD pump lube oil coolers and thrust bearings. The CRD pumps will trip after loss

of RBCCW. The loss of 60 GPM from the CRD system into the reactor cavity will

cause Reactor Cavity and Fuel Pool Levels to slowly lower. RWCU Dump Flow is still

in service and would lower cavity level at the rate of 60 GPM. This question tests

differences between LGS and PBAPS.

Licensees Original Justification for Change

Question Number:

(Missed by all three candidates)

Facility Regrade Request:

Change the correct answer to c

Justification:

It also provides that Control Rod Drive System (CRD) is in service, which provides a normal

flow of approximately 60 gpm to the reactor vessel. With RWCU dump flow out of the reactor

compensating for CRD flow into the reactor, reactor cavity/spent fuel pool level will be stable.

The question then states that both RBCCW pumps trip. The answer key indicates that the

operational implication of this would be that Reactor Cavity and Fuel Pool water level will begin

to lower, which is answer d. The justification for this on the answer key states that The CRD

pumps will trip after a loss of RBCCW. If this were the case and the running RWCU pump

remains running, then reactor cavity/spent fuel pool level would lower.

However, there is no direct trip of the CRD pump due to a loss of RBCCW flow. The PBAPS

Initial Licensed Operator Training lesson plan for Control Rod Drive Hydraulic System, PLOT-

5003A states on page 18 of 24, under Interlocks, that the pump will trip on low suction

pressure and various electrical malfunctions. This is also supported by the Annunciator

Response Card for CRD WATER PUMP TRIP (ARC-211, F-1 and G-1) that lists only Low

suction pressure and Motor overcurrent as the automatic trips of the CRD pumps. The

lesson plan also states (on page 20 of 24) that A loss of TBCCW and RBCCW will cause the

CRD pump to overheat. Therefore, the CRD pump will remain running even with a loss of

TBCCW and RBCCW.

Since RBCCW also cools the RWCU pump motor coolers (see Design Basis Documents P-S-

for RBCCW and P-S-36 for RWCU) a loss of RBCCW will result in an automatic trip of the

RWCU pump due to high temperature in the RWCU pump motor windings at a setpoint of 149

deg.

F. This is supported by ARC-215, A-2 and B-2, which are provided. In addition, the

RWCU System Manager at PBAPS, Luis Feliu (717-456-3634) indicated that this trip would

occur fairly soon after a loss of RBCCW at rated conditions. He also indicated that with the

reactor shutdown and cooled down to a temperature typically seen during a refueling outage,

the high temperature trip setpoint may take longer to reach due to the absence of heat

conduction input from the system, but would still reach the high temperature trip setpoint due to

the heat generated due to the motor winding current. This was also confirmed by the alternate

RWCU System Manager at PBAPS, who was the previous RWCU System Manager, as well as

engineering personnel at LGS, which has similar RWCU pumps. The System Managers also

indicated even with the RPV flooded up to normal level for refueling operations, no dump flow

would be expected after RWCU pump trip, due to the lack of RPV pressure and the high

headloss of the circuitous RWCU dump flowpath (RPV pressure will be approximately 0 psig

since the reactor is in Mode 5 with Core Shuffle Part 1 in progress). When the author of this

question was asked why RWCU was assumed to remain in service, he responded that he

overlooked the high motor winding trip for the RWCU pumps.

The candidates were interviewed to determine why answer c was chosen. The candidates

indicated that they assumed the Fuel Pool Cleanup System was not in service because it was

not stated in the question stem. The candidates also indicated that they were aware of

operational configurations where the Fuel Pool Cleanup System is not in service. The Fuel

Pool Cleanup System is routinely removed from service for other outage related activities (i.e.,

Service Water System maintenance). When the Fuel Pool Cleanup System is removed from

service, the Residual Heat Removal (RHR) System must be placed in service to remove the

decay heat from the reactor cavity and spent fuel pool, as specified in P-S-09, Residual Heat

Removal System. When the RHR System is being used to remove decay heat from the reactor

cavity and spent fuel pool, hot water from the reactor core rises to the surface of the reactor

cavity, flows into the reactor cavity weir opening and through the transfer canal into the fuel

pool, and ultimately flows into the skimmer surge tanks. The water that entered the skimmer

surge tanks is cooled and returned to either the reactor vessel or the spent fuel pool. The

natural circulation currents cause particulate from the reactor cavity to be transported into the

spent fuel pool, degrading overall spent fuel pool water quality. Since none of the particulate is

being removed via the RWCU System, corrosion products will continue to accumulate. These

particles diminish visibility due to the light from the installed spent fuel pool and reactor cavity

lights reflecting off the particles, resulting in the appearance of a haze in the water. The effect

worsens as the particle concentration in the reactor vessel increases.

A loss of RBCCW or RWCU does not require suspension of fuel handling activities, and fuel

movements would continue, causing more corrosion products to be dispersed in the water.

Since the concentration of corrosion product particles will rise in the reactor cavity and spent

fuel pool water when RWCU is out of service, and RWCU pumps will trip, visibility will degrade

over time without RWCU in service. Per OP-PB-112-101-1011, Fuel Handling Director Shift

Turnover Checklist, the LSRO is required to verify once per shift that conditions support error-

free operations, including water clarity. This is required due to the possibility that visibility will

degrade slowly over a period of time, and requires an LSRO to assess conditions at least once

per shift to determine if fuel handling activities may safely continue.

Since the running RWCU pump will trip on high motor winding temperature, and the CRD pump

will not trip, reactor cavity/spent fuel pool level will actually rise very slowly. This makes answer

d incorrect. Also, since the running RWCU pump trips, the clarity of the water in the reactor

cavity/spent fuel pool will degrade, making c the correct answer.

Therefore, the Facility Licensee requests the correct answer for Question 37 be changed to c.

NRC Initial Response

For answer c to be correct, your explanation does not address or explain how the

loss of RWCU (proposed as an explanation for "D" being incorrect) would affect the Fuel Pool

visibility as long as the Fuel Pool Cooling/Cleanup remains in service. Information in the stem

is consistent with Fuel Pool Cooling/Cleanup in service and remaining in service for the duration

of the event. The "normal" configuration during Core Shuffle Part 1 would be to have Fuel Pool

Cooling system in service This system is needed both for decay heat removal and to

establish/maintain clarity in the Fuel Pool. The use of RHR Fuel Pool Cooling assist would NOT

be the "normal" configuration during Core Shuffle Part 1 since it has a tendency to introduce

flow disturbances in the core area. It was also confirmed by Limerick Training that any

scheduled outage of Fuel Pool Cooling would NOT normally be done during Core Shuffle Part

1. Rather it would be done during Core Shuffle Part 2 when there is lower decay heat load.

Excerpts from the System Description for the "Fuel Pool Cooling and Cleanup System", P-S-52,

Revision 5 (provided by the facility licensee) include the following:

1. The Fuel Pool Cooling and Cleanup System has sufficient cooling capacity to maintain the

Spent Fuel Pool water at a temperature at or below 150F for normal decay heat load with two

pumps and two heat exchangers operating.

2. If an abnormally large heat load is placed in the spent fuel pool, a cooling train of the RHR

System consisting of an RHR pump and heat exchanger, is substituted for the Fuel Pool

Cooling pumps and Heat exchangers.for cooling the pool water. The conditions under which

cooling of the Spent Fuel Pool water by the RHR System alone would be required include the

unloading of a full core of irradiated fuel into the pool.

3. Additional heat removal capability may be needed when full core off-loading occurs and less

than three Fuel Pool Cooling Pumps/heat exchangers are available.

4. The service water system shall support operation of the Fuel Pool Cooling System by

providing cooling flow at a rate of 800 GPM.

5. Design basis... minimize corrosion product buildup and control water clarity through filtration

and demineralization.

6. The Fuel Pool Cooling and Cleanup System performs the decay heat removal function

whenever spent fuel is stored in the Spent Fuel Pool, including refueling.

As specified in NUREG -1021, Appendix E. The applicant is directed to ask questions "if you

have any questions concerning the intent or the initial conditions of a question". No applicant

asked any questions regarding question 37 during the exam. The NUREG goes on to specify

that the applicant should "NOT make assumptions regarding conditions that are not specified in

the question unless they occur as a consequence of other conditions that are stated in the

question".

Fuel Pool Cleanup would NOT be lost as a consequence of the loss of RBCCW. It would

appear that the RHR System lineup would only be required if there was a Fuel Pool Cooling

System partial or full outage. There would be normally NO planned outage of Fuel Pool

Cooling during Core Shuffle Part 1. No outage of Fuel Pool Cooling equipment was specified in

the stem. Nor was there any mention of a "full core off-load". Therefore, the applicant would

have no technical basis for assuming that Fuel Pool Cleanup was either NOT running at the

onset, nor for assuming it was lost following the event. Therefore, as presented in your

submittal, there appears to be no basis for concluding that the stem conditions would result in

degrading Fuel Pool visibility.

Revised and Final Facility Regrade Request:

Change the correct answer to c.

Justification:

The question provides that Reactor Building Closed Cooling Water System (RBCCW) is

backing up Turbine Building Closed Cooling Water System (TBCCW), and Reactor Water

Cleanup (RWCU) is dumping 60 gpm to the main condenser. It also provides that Control Rod

Drive System (CRD) is in service, which provides a normal flow of approximately 60 gpm to the

reactor vessel. With RWCU dump flow out of the reactor compensating for CRD flow into the

reactor, reactor cavity/spent fuel pool level will be stable.

The question then states that both RBCCW pumps trip. The original answer key indicates that

the operational implication of this would be that Reactor Cavity and Fuel Pool water level will

begin to lower, which is answer d. The justification for this on the answer key states that The

CRD pumps will trip after a loss of RBCCW. If this were the case and the running RWCU

pump remains running, then reactor cavity/spent fuel pool level would lower.

However, there is no direct trip of the CRD pump due to a loss of RBCCW flow. The PBAPS

Initial Licensed Operator Training lesson plan for Control Rod Drive Hydraulic System, PLOT-

5003A states on page 18 of 24, under Interlocks, that the pump will trip on low suction

pressure and various electrical malfunctions. This is also supported by the Annunciator

Response Card for CRD WATER PUMP TRIP (ARC-211, F-1 and G-1) that lists only Low

suction pressure and Motor overcurrent as the automatic trips of the CRD pumps. The

lesson plan also states (on page 20 of 24) that A loss of TBCCW and RBCCW will cause the

CRD pump to overheat. Therefore, the CRD pump will remain running even with a loss of

TBCCW and RBCCW.

Since RBCCW also cools the RWCU pump motor coolers (see Design Basis Documents

P-S-33 for RBCCW and P-S-36 for RWCU) a loss of RBCCW will result in an automatic trip of

the RWCU pump due to high temperature in the RWCU pump motor windings at a setpoint of

149 deg.

F. This is supported by ARC-215, A-2 and B-2, which are provided. In addition, the

RWCU System Manager at PBAPS, indicated that this trip would occur fairly soon after a loss

of RBCCW at rated conditions. He also indicated that with the reactor shutdown and cooled

down to a temperature typically seen during a refueling outage, the high temperature trip

setpoint may take longer to reach due to the absence of heat conduction input from the system,

but would still reach the high temperature trip setpoint due to the heat generated due to the

motor winding current. This was also confirmed by the alternate RWCU System Manager at

PBAPS, who was the previous RWCU System Manager, as well as engineering personnel at

LGS, which has similar RWCU pumps. The System Managers also indicated even with the

RPV flooded up to normal level for refueling operations, no dump flow would be expected after

RWCU pump trip, due to the lack of RPV pressure and the high headloss of the circuitous

RWCU dump flowpath (RPV pressure will be approximately 0 psig since the reactor is in Mode

with Core Shuffle Part 1 in progress). When the author of this question was asked why

RWCU was assumed to remain in service, he responded that he overlooked the high motor

winding trip for the RWCU pumps. Since RWCU will trip, and CRD may or may not trip, reactor

cavity and spent fuel pool level will not lower, therefore, answer d is not correct.

Spent fuel bundles are covered with a loose coating of corrosion products. Some of these

corrosion products will easily detach from the bundles when they are moved through the water.

With fuel shuffle part 1 in progress, corrosion products will be deposited in the reactor cavity

water as the bundles are removed from the core. Documentation of this is seen in the

Operations Narrative Logs from PBAPS Refueling Outage 3R14. At 2032 on 9/21/2003, Fuel

Shuffle Part 1 commenced. While this log entry does not specify this Fuel Shuffle as being

Part 1, subsequent log entries at 2356 on 9/21/2003 and 0430 on 9/22/2003 confirm this as

being Shuffle Part 1. The only activities scheduled to be performed in the reactor vessel during

Shuffle Part 1 are fuel movements and some in-vessel visual inspection activities. At 0122 on

9/23/2003, RHR Shutdown Cooling was removed from service temporarily for fuel pool clarity.

When RHR is in operation in normal Shutdown Cooling mode or Fuel Pool to Reactor Mode,

the discharge of the operating RHR pump is to the bottom head area via the jet pump

discharge. The forced flow of water upward through the reactor tends to push corrosion

products up, where RWCU has difficulty removing it. Removal of shutdown cooling is one

option to allow the corrosion products to be drawn down to the RWCU pump suctions from the

recirculation piping and the bottom head drain. This series of log entries shows a degradation

in clarity as Fuel Shuffle Part 1 progresses. The effect is obviously worsened if RWCU trips

and is out of service, since no removal of corrosion products will occur down in the reactor core

area. The RWCU trip results in a reduction in filtration of the reactor cavity water, resulting in a

higher concentration of corrosion products, and a degradation of the visibility of the reactor

cavity water. Simply put, if the initial conditions assume a given amount of filtration, and some

of that filtration is lost, less corrosion particles will be removed, and visibility will degrade.

Furthermore, the only filtration system that may still be in service takes water only from the

surface of the reactor cavity, spent fuel pool, and equipment pit. Any corrosion products in the

water are required to travel to the surface to be removed. These particles diminish visibility due

to the light from the installed spent fuel pool and reactor cavity lights reflecting off the particles,

resulting in the appearance of a haze in the water. The effect worsens as the particle

concentration increases. Since the fuel handling crew on the refuel platform is now required to

look through more corrosion products in the water, visibility is degraded.

As shown on PBAPS P&ID M-363, sheet 1, water flows from the reactor cavity, spent fuel pool,

and equipment pit to the skimmer surge tanks. Since each of these three bodies of water have

four returns to the skimmer surge tanks and are at the same height, an approximately equal

amount of water flows from each area to the skimmer surge tanks. The typical fuel pool cooling

alignment for Core Shuffle Part 1 is two or three fuel pool cooling pumps, heat exchangers, and

demineralizers. Peach Bottom procedure SO 19.1.A-2, Fuel Pool Cooling System Startup and

Normal Operations, specifies in step 4.1.15.4 that a maximum flowrate of 550 gpm is permitted

through each demineralizer. For example, if two demineralizers are in service, the maximum

combined flowrate through the demineralizers is 1100 gpm. If SO 19.7.E-2, Aligning Fuel Pool

Cooling System to Reactor Well, is performed, the return flow from the Fuel Pool Cooling

System is split between the spent fuel pool and the reactor cavity. Since both the spent fuel

pool and reactor cavity each have two 6-inch returns, it can be assumed that approximately the

same flow returns to each area. This means that with two Fuel Pool Cooling pumps in service,

550 gpm would return to each area. This was the alignment for Fuel Shuffle Part 1 during the

last PBAPS refueling outage, as shown in the attached Operations Narrative Logs from PBAPS

Refueling Outage 2R15. The entry at 1135 a.m. on 9/16/2004 shows two Fuel Pool Cooling

pumps, heat exchangers, and demins are in service, and aligned for return to both the spent

fuel pool and reactor cavity per SO 19.7.E-2.

The RHR system alignment used during the entire Shuffle Part 1 for PBAPS 2R15 was Fuel

Pool to Reactor Mode per AO 10.4-2, with a flowrate of 5000 gpm. This is a common mode,

and depending on work that must be performed, can be the mode used for the majority of the

outage. It is used extensively at both LGS and PBAPS. AO 10.4-2 aligns the operating RHR

pump suction from the skimmer surge tanks, and discharges to the reactor vessel via the

normal shutdown cooling discharge flowpath. The Narrative Logs show the RHR system was

placed in this mode at 0401 a.m. on 9/17/2004, approximately one hour before the start of

Shuffle Part 1. RHR was maintained in this alignment until long after Shuffle Part 1 was

completed.

Since the RHR pump is drawing 5000 gpm from the skimmer surge tanks, and the Fuel Pool

Cooling system is drawing another 1100 gpm from the skimmer surge tanks, a total of 6100

gpm flows into and out of the skimmer surge tanks. Since about one-third of this flow (about

2000 gpm) is coming from the spent fuel pool, and only about 550 gpm of flow returning from

the Fuel Pool Cooling system is returning to the spent fuel pool, then about 1450 gpm must flow

from the reactor cavity to the spent fuel pool. The assumption that at least one-third of the

water flowing into the skimmer surge tanks is from the spent fuel pool is a valid assumption,

since the surface area of the spent fuel pool is slightly greater than one-third of the total surface

area, and the weir plates will be adjusted to be consistent between the pools. According to Bill

Bianco, Outage Services Engineer, surface areas of the three pools of water are as follows:

Spent Fuel Pool - 616 sq. ft.

Reactor Cavity - 550 sq. ft.

Equipment Pit - 602 sq. ft.

It is impossible for all 2000 gpm of the flow out of the spent fuel pool to come strictly from spent

fuel pool water. Since only about 550 gpm is returning to the spent fuel pool from the Fuel Pool

Cooling system, the only place the other 1450 gpm can come from is from the reactor cavity

through the transfer canal. It is also not possible for more water to flow from the reactor cavity

into the skimmer surge tanks than from the spent fuel pool. Per AO 10.4-2, step 4.1.4, the fuel

pool to skimmer surge tank weir gates and reactor cavity to skimmer surge tank weir gates are

in their lowest position. This is also required per SO 19.7.E-2. Since the weir plates in the

reactor cavity match the level of the skimmer surge tank weirs on the spent fuel pool side, level

would have to be higher in the reactor cavity to have higher flow. Since both bodies of water

are connected through the transfer canal, it is not possible for them to be at different heights.

The significant amount of water flowing through the transfer canal from the reactor cavity into

the spent fuel pool brings the degraded water from the reactor cavity into the spent fuel pool,

causing its water to also degrade. Even when Fuel Pool Cooling is in service, the degradation

will slowly worsen over time, as only about 370 gpm of the flow from the spent fuel pool (one-

third of 1100) is filtered by the Fuel Pool Cooling demineralizers.

The attached Operations Narrative Logs from the most recent PBAPS Refueling outage (2R15)

is provided in support of the above statements.

In summary, since the running RWCU pump will trip on high motor winding temperature, and

the CRD pump may or may not trip on overcurrent due to high temperature, reactor cavity/spent

fuel pool level will either not change (if CRD trips), or will rise very slowly (if CRD does not trip).

In either case, this makes answer d incorrect. A loss of RWCU during Shuffle Part 1 will

cause degradation of reactor cavity water, and with RHR in Fuel Pool to Reactor mode, which is

a typical mode during refueling outages, spent fuel pool water visibility would also degrade.

This makes answer c the correct answer. Answer c must be considered a valid answer,

since if the exact same situation had actually occurred at any time during Shuffle Part 1 of the

last PBAPS refueling outage, reactor cavity and spent fuel pool visibility would have degraded

as a result of the RHR alignment being used, regardless of whether Fuel Pool Cooling was in

service or not.

Therefore, the Facility Licensee requests the correct answer for Question 37 be changed to c.

References Provided:

  • Design Basis Document P-S-33, Reactor Building Closed Cooling Water System
  • MCR ARC-211, G-1
  • MCR ARC-215, A-2 and B-2
  • SO 19.7.E-2, Aligning Fuel Pool Cooling System to Reactor Well
  • SO 19.1.A-2, Fuel Pool Cooling System Startup and Normal Operations
  • Peach Bottom Archival Operations Narrative Logs for period of 9/20/2003 through

9/23/2003

  • Peach Bottom Archival Operations Narrative Logs for period of 9/15/2004 through

9/20/2004

NRC Final Resolution:

The NRC agrees with and accepts the licensees recommendation to change the correct

answer from d to c. The NRC conducted detailed reviews of all references provided. As a

result of spent fuel bundles movements some corrosion products will detach from the bundles

when they are moved through the water and will be deposited in the reactor cavity. Over time a

trip of the RWCU pump will result in a degradation of the visibility of the reactor cavity water

due to a reduction in filtration of the reactor cavity water. Furthermore, the Fuel Pool Cooling

system takes water only from the surface of the reactor cavity, spent fuel pool, and equipment

pit. Any corrosion products in the water are required to travel to the surface to be removed.

Even with the Fuel Pool Cooling is in service, the degradation will slowly worsen over time. The

system line-ups described in the licensees submittal would cause a significant flow of water

through the transfer canal from the reactor cavity into the spent fuel pool. The degraded water

from the reactor cavity would enter the spent fuel pool, therefore, over time the water visibility in

both the reactor cavity and the spent fuel pool would be expected to degrade. A loss of RWCU

during Shuffle Part 1 will cause degradation of reactor cavity water, and with RHR in Fuel Pool

to Reactor mode, which is a typical mode during refueling outages, spent fuel pool water

visibility would also degrade. This makes answer c the correct answer.

Answer d cannot be correct since the CRD pump is expected to continue to run after loss of

RBCCW and after the (relatively fast) trip of the RWCU pump. The CRD pump is adding 60

GPM to the reactor cavity (and connected fuel pool). The RWCU pump is required to be

running to effect a 60 GPM dump flow to the condenser. In this instance (with CRD pump

running and RWCU pump tripped), the Reactor Cavity and Fuel Pool levels would actually

increase (making D wrong from the onset). In addition, in response to the RWCU pump trip

annunciator (ARC # 215), the control room personnel will Shutdown the RWCU system in

accordance with SO 12.2.A-2, Reactor Water Cleanup System Shutdown.

There is no direct trip of the CRD pump from loss of RBCC

W. However, loss of RBCCW will

cause the CRD pump to overheat. This overheating condition may (in the long term) cause a

pump trip. However, in the worst case, after all RWCU and CRD pumps (eventually) trip, the

Reactor Cavity and Fuel Pool levels will remain constant. In NO instance would the level begin

to lower.

Answer a cannot be correct since there is no increase in activity and no mechanism to spread

the existing activity to other areas of the plant. With the RWCU pump tripped all activity in the

RCS will remain in the RCS and there will be NO higher than normal plant dose rates.

Answer b cannot be correct since, as stated in the original question explanation, PBAPS

Refueling Bridge has an independent self-cooled air compressor that has no connection with

the station air system(s) and no connection with RBCCW.

Conclusion

The NRC accepts the licensees comment to change the correct answer for Question #37

from D to C.

Original LSRO Question #26:

A nuclear reactor has been shutdown for one week from long-term power operation and

shutdown cooling is in service. Upon loss of cooling water to the shutdown cooling heat

exchangers, which one of the following coefficients of reactivity will act first to change core

reactivity and determine the effect on Shutdown Margin? (Assume continued forced circulation

through the core)

Coefficient to Act First Effect on Shutdown Margin

C. Moderator temperature coefficient Decrease

D. Fuel temperature coefficient Increase

E. Fuel temperature coefficient Decrease

F. Moderator Temperature coefficient Increase

Originally designated correct answer A.

Submitted answer explanation:

Note: Question #26 was significantly modified from the original draft question due to a K/A

mismatch problem. The replacement question did not provide any documented justification for

the correct answer, nor any explanation about why the three distractors were incorrect. The

licensee exam developer confirmed he had intended to change the designated correct answer,

after revising the question, but did not follow through with this intent.

LICENSEES JUSTIFICATION FOR CHANGE:

Revised answer explanation:

Facility Regrade Request:

Accept d as the correct answer.

Justification:

This question was modified from NRC Generic Fundamentals Examination Question Bank

question B52.

The question provides a reactor shutdown for one week from long-term power operation and

shutdown cooling in service. It then provides that cooling water is lost to the shutdown cooling

heat exchangers. The candidate is then asked to determine which coefficient of reactivity will

act first to change core reactivity and what the effect will be on Shutdown Margin.

The given answer on the answer key provides that moderator temperature coefficient will be the

first to act. The Facility Licensee agrees that moderator temperature coefficient will act first,

since moderator temperature will rise as a direct result of the loss of cooling to the RHR heat

exchangers. The candidate must now decide if this will result in a decrease in Shutdown

Margin (choice a), or an increase in shutdown margin (choice d).

For most of the core life, the reactor is considered to have a negative moderator temperature

coefficient, where the effect of increasing moderator temperature will be to add negative

reactivity to the core. This is due to the moderator density decreasing as a result of the

temperature increase, causing neutrons to travel farther before slowing down to thermal

energies, and having a higher probability of resonant absorption. Since more neutrons undergo

resonant absorption, fewer neutrons are available for thermal fission, and the effect is to add

negative reactivity to the core. This addition of negative reactivity moves the reactor farther

from criticality, which increases Shutdown Margin. This would make d the correct answer.

If the assumption is made that the core is at the end of life with low moderator temperature, the

reactor could have a positive moderator temperature coefficient, which will result in the addition

of positive reactivity as moderator temperature is increased. This occurs because as moderator

temperature rises, less moderator atoms are present in the core to compete with the fuel for the

thermal neutrons. This causes the thermal utilization factor to increase, resulting in more

thermal neutrons available to cause fission in the fuel. The addition of positive reactivity moves

the reactor closer to criticality, which decreases Shutdown Margin. This would make a the

correct answer.

Upon further investigation, information was obtained from LaSalle on reactivity effects of

moderator temperature at various points in core life. This information is not normally calculated

for Limerick or Peach Bottom, but LaSalle is very similar as a C- lattice plant with 764 fuel

bundles and 185 control rods. Core response at Limerick and Peach Bottom would therefore

also behave in a similar fashion.

As can be seen in the attached spreadsheets for various times in core life, the moderator

temperature coefficient can become positive as fuel exposure increases at low moderator

temperatures. This is common for BWR plants and can have operational impacts under these

special conditions. However, under all rod in conditions, such as during an outage, the

moderator temperature coefficient is always negative. This can be seen on the attached

spreadsheets since the curve for the ARI condition never crosses the 0.000 reactivity point.

This is true for all exposure values calculated and for all temperatures. Based upon this data,

answer a cannot be correct.

Therefore, the Facility Licensee requests d be accepted as the correct answer.

References Provided:

  • General Physics BWR Generic Fundamentals Reactor Theory Student Text, Chapter 2

(Neutron Life Cycle)

  • General Physics BWR Generic Fundamentals Reactor Theory Student Text, Chapter 4

(Reactivity Coefficients)

B1248, B1752, B3652.

LaSalle spreadsheets of reactivity variations with moderator temperature at various times in

core life (attached).

Licensees Conclusion: Change the correct answer from A to D.

NRC RESOLUTION:

The NRC agrees with and accepts the licensees recommendation.

The actual training provided to the applicants (page 25 of BWR Reactor Theory, Chapter 2)

specifies:

The following parameters or design features affect shutdown reactivity conditions:

  • Moderator temperature- An increase inserts negative reactivity, increasing the shutdown

margin . . .

This training justifies D as a correct answer. This is also technically correct as explained in

the licensees letter.

The context of this statement in Chapter 2 is based on a reactor being undermoderated and

having a negative moderator temperature coefficient of reactivity. This is true for over 90% of

the core life. For over-moderated reactors having a positive moderator temperature coefficient

of reactivity, the opposite effect (decrease in Shutdown Margin) will be manifested by a loss of

cooling to the shutdown cooling heat exchanger. As specified on page 5 of BWR Reactor

Theory, Chapter 4, the potential exists for the occurrence of a positive moderator temperature

coefficient of reactivity This is shown to occur late in core life at temperatures between 100 F

and 200

F. Since there was no specified core life in the stem of the question, and in the context

of a LSRO (performing refueling outages) it would be reasonable for an applicant to conclude

end of core life conditions prevailed.

In this instance (with a positive temperature coefficient at EOL), A would be technically

justified as the correct answer.

However, it has been demonstrated that the Limerick and Peach Bottom cores would NEVER

be in an over-moderated condition with all rods in. Since the stem provided that the reactor

has been shutdown for one week the applicant should conclude all rods are in. Therefore,

answer A cannot be correct.

There is a direct training basis for selecting D as the correct answer. There is a technically

accurate core physics basis for selecting D as the correct answer. There is NO technically

accurate core physics basis for selecting A as a correct answer. Therefore, there is a basis

for selecting only D as a correct answer.

Conclusion:

Accept the licensees recommendation to change the correct answer from A to D for

LSRO Question #26. The NRC will change the master grading sheet accordingly and

regrade all applicants using the revised grading sheet.

A2-14