BSEP-87-1079, Special Rept 2-SR-87-001:on 870824,Unit 2 Fire Barrier Limiting Condition for Operation Was Initiated on Fire Door 003 as Door Would Not Close & Latch Properly.Cause Not Stated.Door Repaired & Returned to Svc
ML20235H290 | |
Person / Time | |
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Site: | Brunswick |
Issue date: | 09/22/1987 |
From: | Dietz C CAROLINA POWER & LIGHT CO. |
To: | Grace J NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
References | |
2-SR-87-001, 2-SR-87-1, BSEP-87-1079, NUDOCS 8710010005 | |
Download: ML20235H290 (1) | |
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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO LER)
MONTHYEARBSEP-98-0210, Special Rept:On 980824,temp Element 2-CAC-TE-1258-22 Failed. Cause of Failed Temp Element Cannot Be Conclusively Determined.Temp Element Will Be Replaced & Cable Connections Repaired1998-10-30030 October 1998
[Table view]Special Rept:On 980824,temp Element 2-CAC-TE-1258-22 Failed. Cause of Failed Temp Element Cannot Be Conclusively Determined.Temp Element Will Be Replaced & Cable Connections Repaired BSEP-94-0103, Special Rept 1-SR-94-002:on 940226,fire Barrier Penetration Between EDG Bldg & Diesel Fuel Oil Day Storage Tank Room Opened.Fire Watch Stationed Prior to Opening Penetration & Remained in Place Until Penetration Fire Seal Operable1994-03-18018 March 1994 Special Rept 1-SR-94-002:on 940226,fire Barrier Penetration Between EDG Bldg & Diesel Fuel Oil Day Storage Tank Room Opened.Fire Watch Stationed Prior to Opening Penetration & Remained in Place Until Penetration Fire Seal Operable BSEP-93-0238, Special Rept SR 1-93-013:on 931117,fire Protection LCO A1-93-F0859 Initiated on Fire Seal R1-2-077.Seal Inoperable to Facilitate Overspeed Trip Setting Testing of HPCI & RCIC Sys.Fire Seal Restored on 9312041993-12-22022 December 1993 Special Rept SR 1-93-013:on 931117,fire Protection LCO A1-93-F0859 Initiated on Fire Seal R1-2-077.Seal Inoperable to Facilitate Overspeed Trip Setting Testing of HPCI & RCIC Sys.Fire Seal Restored on 931204 BSEP-93-0011, Special Rept 1-SR-93-001:on 921216,reactor Bldg Fire Detection Sys Declared Inoperable Due to Continuous Spurious Alarming in Ionization Detectors for More than 14 Days. Sensitivity Testing & Cleaning Implemented1993-01-29029 January 1993 Special Rept 1-SR-93-001:on 921216,reactor Bldg Fire Detection Sys Declared Inoperable Due to Continuous Spurious Alarming in Ionization Detectors for More than 14 Days. Sensitivity Testing & Cleaning Implemented BSEP-93-0005, Special Rept 1-SR-93-002:on 930107,both Fire Suppression Sys Fire Pumps Were Made Inoperable to Allow Replacement of Isolation Valve.Personnel Were Stationed to Monitor Diesel Fire Pump Operation1993-01-19019 January 1993 Special Rept 1-SR-93-002:on 930107,both Fire Suppression Sys Fire Pumps Were Made Inoperable to Allow Replacement of Isolation Valve.Personnel Were Stationed to Monitor Diesel Fire Pump Operation BSEP-93-0007, Special Rept 1-SR-93-002:on 930116,both Fire Suppression Sys Fire Pumps Will Be Made Inoperable for Approx 8 H to Allow Replacement of Isolation Valve (2-FP-V79).Personnel Will Be Stationed to Monitor Diesel Fire Pump Operation1993-01-15015 January 1993 Special Rept 1-SR-93-002:on 930116,both Fire Suppression Sys Fire Pumps Will Be Made Inoperable for Approx 8 H to Allow Replacement of Isolation Valve (2-FP-V79).Personnel Will Be Stationed to Monitor Diesel Fire Pump Operation BSEP-93-0003, Special Rept 1-SR-93-002:on 930107 Both Fire Suppression Sys Fire Pumps Will Be Made Inoperable for Approx 8 H to Permit Replacement of Isolation Valve & Associated Instrument Line. Personnel Will Monitor Diesel Fire Pump Operation1993-01-0606 January 1993 Special Rept 1-SR-93-002:on 930107 Both Fire Suppression Sys Fire Pumps Will Be Made Inoperable for Approx 8 H to Permit Replacement of Isolation Valve & Associated Instrument Line. Personnel Will Monitor Diesel Fire Pump Operation BSEP-92-0054, Special Rept 1-SR-92-010:on 921130,makeup Water Treatment Area Sprinkler Sys Declared Inoperable.On 921212,DG Bldg Southwest Switchgear Room Inoperable.On 921216,Unit 1 Air Lock Doors Blocked Open.On 921217,RWCU Barrier Inoperable1993-01-0606 January 1993 Special Rept 1-SR-92-010:on 921130,makeup Water Treatment Area Sprinkler Sys Declared Inoperable.On 921212,DG Bldg Southwest Switchgear Room Inoperable.On 921216,Unit 1 Air Lock Doors Blocked Open.On 921217,RWCU Barrier Inoperable ML20125C5921992-12-0404 December 1992 Special Rept 1-SR-92-009:on 921031,EDG Bldg 23 Elevation Fire Barrier Doors 108 & 120 Declared Inoperable.Doors Did Not Completely Auto Close After Normal pass-through.Repairs Delayed Due to Unavailability of Replacement Doors BSEP-92-0036, Special Rept 1-SR-92-008:on 921007 & 09 EDG Bldg 50 Feet Elevation Fire Barrier Seals DG-3-437,472 & 473 Declared Inoperable,Respectively to Support Plant Mod 92-069.Seals Will Be Restored Prior to Startup of Either Unit1992-11-10010 November 1992 Special Rept 1-SR-92-008:on 921007 & 09 EDG Bldg 50 Feet Elevation Fire Barrier Seals DG-3-437,472 & 473 Declared Inoperable,Respectively to Support Plant Mod 92-069.Seals Will Be Restored Prior to Startup of Either Unit BSEP-92-0026, Special Rept 1-SR-92-007:on 920919,conduit Leading to Seal AO-3-014 on Augmented Offgas 50-ft Elevation Declared Inoperable Due to Corrosion at Floor Penetration.Fire Watch Stationed Until Restoration of Fire Barrier Seal1992-10-21021 October 1992 Special Rept 1-SR-92-007:on 920919,conduit Leading to Seal AO-3-014 on Augmented Offgas 50-ft Elevation Declared Inoperable Due to Corrosion at Floor Penetration.Fire Watch Stationed Until Restoration of Fire Barrier Seal BSEP-92-0025, Special Rept 2-SR-92-008:on 920909,crack Found in Thermo-Lag of Penetration Seal in Control Bldg Cable Spread Room During Review of NRC Bulletin 92-001.Seal Not Restored within 7 Days.Fire Watches Stationed in Affected Areas1992-10-12012 October 1992 Special Rept 2-SR-92-008:on 920909,crack Found in Thermo-Lag of Penetration Seal in Control Bldg Cable Spread Room During Review of NRC Bulletin 92-001.Seal Not Restored within 7 Days.Fire Watches Stationed in Affected Areas BSEP-92-0022, Special Rept 1-SR-92-006:on 920904 & 21,secondary Containment Airlock Doors Both Opened to Support Increased Traffic During Outage & Not Restored within 7 Days.Fire Watch Stationed & Remained in Place Until Barrier Restored1992-10-12012 October 1992 Special Rept 1-SR-92-006:on 920904 & 21,secondary Containment Airlock Doors Both Opened to Support Increased Traffic During Outage & Not Restored within 7 Days.Fire Watch Stationed & Remained in Place Until Barrier Restored BSEP-92-0013, Special Rept 2-SR-92-007:on 920823,fire Door 206 on 50-ft Elevation of EDG Bldg Declared Inoperable.Caused by Fire Door Not Latching Consistently Due to Broken Springs.Latch Repaired & Fire Watch Stationed in Area1992-09-28028 September 1992 Special Rept 2-SR-92-007:on 920823,fire Door 206 on 50-ft Elevation of EDG Bldg Declared Inoperable.Caused by Fire Door Not Latching Consistently Due to Broken Springs.Latch Repaired & Fire Watch Stationed in Area ML20105B2461992-09-14014 September 1992 Special Rept:On 920810,fire Barrier Between Control Bldg Stairwell & 23-ft Elevation Cable Spread Room Declared Inoperable to Support Planned Mod.Hourly Fire Watch Will Remain in Place Pending Restoration of Fire Barrier BSEP-92-0006, Special Rept 2-SR-92-006:on 920729,fire Doors in CR Stairwell Area Declared Inoperable to Perform Plant Mod.On 920731,secondary Containment Airlock Doors Both Opened.Fire Watch Stationed,Pending Restoration of Fire Door1992-09-0303 September 1992 Special Rept 2-SR-92-006:on 920729,fire Doors in CR Stairwell Area Declared Inoperable to Perform Plant Mod.On 920731,secondary Containment Airlock Doors Both Opened.Fire Watch Stationed,Pending Restoration of Fire Door BSEP-92-0002, Special Rept 1-SR-92-004:on 920706,control Bldg Computer Room Fire Door Propped Open & Declared Inoperable.On 920709, Containment Airlock Doors Opened for More than 7 Days.Fire Watch Stationed & Remains in Place Pending Restoration1992-08-12012 August 1992 Special Rept 1-SR-92-004:on 920706,control Bldg Computer Room Fire Door Propped Open & Declared Inoperable.On 920709, Containment Airlock Doors Opened for More than 7 Days.Fire Watch Stationed & Remains in Place Pending Restoration BSEP-92-0005, Special Rept 2-SR-92-005:on 920706,fire Barrier Penetration Seal in Reactor Bldg ECCS Piping Room Declared Inoperable. LCO Expected to Expire Before Repairs Completed.Fire Watch Established & Remains in Place Pending Replacement of Seal1992-08-10010 August 1992 Special Rept 2-SR-92-005:on 920706,fire Barrier Penetration Seal in Reactor Bldg ECCS Piping Room Declared Inoperable. LCO Expected to Expire Before Repairs Completed.Fire Watch Established & Remains in Place Pending Replacement of Seal ML20101R1911992-07-10010 July 1992 Special Rept 2-SR-92-004:on 920603,05 & 06,LCOs Initiated Due to Open Fire Barrier Penetration Seal,Hole in East Wall of Reactor Bldg & Opening of Fire Door 102,respectively.Fire Watches Established & Penetration Seal Restored ML20097D7331992-06-0505 June 1992 Special Rept 2-SR-92-003:on 920507,08,10,12,15,27 & 29 LCO Exceeded Time Estimated for Completion of Work Initiated. Appropriate Fire Watches Established During Stated Times ML20098D8301992-05-22022 May 1992 Special Rept 1-SR-92-002:on 920421,7-day LCO Initiated Due to Fire Door 115 Being Opened to Accommodate Outage Work. on 920430,7-day LCO Initiated Due to Interlock on Fire Door 203 Being Placed Under Clearance to Support Outage Work ML20096E0361992-05-0808 May 1992 Special Rept 2-SR-92-002:on 920324,generated LCO for Radioactive Gaseous Effluent Monitoring Instrumentation Incomplete in That Requirements of TS 3.3.5.3 Not Invoked. Monitor Inoperable for More than 7 Days ML20092M1861992-02-24024 February 1992 Special Rept:On 920113,inoperable Fire Detectors in Zone 14 Identified.Caused by Lack of Replacement Detectors.Work Order Initiated to Repair Detector ML20092M9961992-02-24024 February 1992 Special Rept 1-SR-92-001:on 920109,14-day LCO Initiated Due to Inoperable Fire Detectors in Zone 14.Replacement Detectors Installed on 920207.On 920119 14-day LCO Exceeded Due to Inoperable Fire Detectors in Zone 10 ML20091P4451992-01-27027 January 1992 Special Rept 1-92-001:on 920106,main Turbine Stop Valve Limit Switch Failure Resulted in Inadvertent Primary Electrical Lockout Which Initiated Auto Start Signal to All EDGs ML20086S8281991-12-27027 December 1991 Ro:On 910822,indefinite Primary Containment Isolation Sys TS Limiting Condition for Operation Occurred After Unsuccessful Attempts to Quantify Leakage on-line.Caused by Mfg Flaws in Lower Wedge of Stanchion.Upper & Lower Wedges Replaced ML20091G7021991-12-12012 December 1991 Special Rept:On 911112,14-day LCO on Fire Detection Instrumentation for Reactor Bldg Refuel Floor Expired.Lco Not Cancelled within 14-day Time Period Since Source of Spurious Alarms Could Not Be Determined.Sys to Be Replaced ML20085K5071991-10-25025 October 1991 Special Rept 2-SR-91-003:on 910919,LCO Initiated Due to Removal of North Hatch on ECCS mini-steam Tunnel Roof in Reactor Bldg.On 911004,LCOs Initiated to Open Penetrations. Appropriate Fire Watches Established ML20082P8941991-09-0505 September 1991 Special Rept:On 910722,seismic Monitoring Triaxial time-history Accelograph 2ENV-XT-823-2 Found Inoperable. Preliminary Trouble Shooting Indicated Open Circuit in Connector.Repair Deferred Until Refueling Outage Scheduled ML20077G9491991-06-26026 June 1991 Special Rept 1-SR-91-003:on 910527,7-day Limiting Condition for Operation Exceeded to Repair Latching Mechanism on Fire Door 303 at Penetration Seal R1-3-009.Door Repaired & Fire Watches Maintained BSEP-91-0177, Special Rept 1-SR-91-001:on 910326,limiting Conditions for Operation Initiated Due to Inoperable Fire Doors.Caused by Routine Usage.Fire Doors 207,107 & 214 Repaired & Restored on 910402.Station Fire Watches Were Maintained1991-04-25025 April 1991 Special Rept 1-SR-91-001:on 910326,limiting Conditions for Operation Initiated Due to Inoperable Fire Doors.Caused by Routine Usage.Fire Doors 207,107 & 214 Repaired & Restored on 910402.Station Fire Watches Were Maintained BSEP-91-0020, Special Rept 1-SR-90-005:on 901130,Zone 1 of Svc Water Bldg Fire Detection Sys Declared Inoperable Due to Spurious Alarms on Main Control Room Annunicator.Caused by Defective Pull Station.Fire Detection Panel Replaced1991-01-10010 January 1991 Special Rept 1-SR-90-005:on 901130,Zone 1 of Svc Water Bldg Fire Detection Sys Declared Inoperable Due to Spurious Alarms on Main Control Room Annunicator.Caused by Defective Pull Station.Fire Detection Panel Replaced BSEP-90-0827, Special Rept 1-SR-90-004:on 901121,7-day Time Frame of LCO Exceeded.Caused by Fire Barrier Penetration Seal Out of Svc for Inservice Insp Work.Until Work Completed,Hourly Fire Watch Patrol Will Remain in Effect1990-12-20020 December 1990 Special Rept 1-SR-90-004:on 901121,7-day Time Frame of LCO Exceeded.Caused by Fire Barrier Penetration Seal Out of Svc for Inservice Insp Work.Until Work Completed,Hourly Fire Watch Patrol Will Remain in Effect BSEP-90-0799, Special Rept 1-SR-90-003:on 901016,reactor Bldg Fire Detection Sys Zone 14 Instrumentation Declared Inoperable. Hourly Fire Watch Patrol in Effect1990-11-29029 November 1990 Special Rept 1-SR-90-003:on 901016,reactor Bldg Fire Detection Sys Zone 14 Instrumentation Declared Inoperable. Hourly Fire Watch Patrol in Effect BSEP-90-0782, Special Rept 1-SR-90-002:on 901028,7-day Time Frame of LCO Exceeded for Fire Door 203.Fire Watches Remained Stationed Until LCO Canceled on 9010291990-11-21021 November 1990 Special Rept 1-SR-90-002:on 901028,7-day Time Frame of LCO Exceeded for Fire Door 203.Fire Watches Remained Stationed Until LCO Canceled on 901029 BSEP-89-0766, Special Rept 2-SR-89-003:on 890731,fire Barrier Limiting Condition for Operation Initiated for Door 301 to Permit Frame & Door Replacement to Correct Misalignment & Sticking Problem.Time Frame Exceeded.Restoration Expected by 8909081989-08-15015 August 1989 Special Rept 2-SR-89-003:on 890731,fire Barrier Limiting Condition for Operation Initiated for Door 301 to Permit Frame & Door Replacement to Correct Misalignment & Sticking Problem.Time Frame Exceeded.Restoration Expected by 890908 BSEP-89-0735, Special Rept 2-SR-89-002:on 890717,fire Barrier Limiting Condition for Operation Initiated to Allow Replacement of Door & Door Frame to Correct Misalignment & Sticking Problem.Time Frame Exceeded.Restoration Expected by 8908311989-08-0101 August 1989 Special Rept 2-SR-89-002:on 890717,fire Barrier Limiting Condition for Operation Initiated to Allow Replacement of Door & Door Frame to Correct Misalignment & Sticking Problem.Time Frame Exceeded.Restoration Expected by 890831 BSEP-89-0637, Special Rept 1-SR-89-002:on 890606,fire Barrrier Limiting Condition for Operation Initiated for Fire Door 303 to Permit Replacement of Door & Frame to Correct Misalignment & Sticking1989-06-30030 June 1989 Special Rept 1-SR-89-002:on 890606,fire Barrrier Limiting Condition for Operation Initiated for Fire Door 303 to Permit Replacement of Door & Frame to Correct Misalignment & Sticking BSEP-89-0494, Special Rept 2-SR-89-001:on 890422,limiting Condition for Operation Initiated Due to Two Inoperable Fire Barrier Penetration Seals in Common Augmented Offgas Bldg.On 890429, 7-day Time Frame Exceeded.Work Request Initiated1989-05-24024 May 1989 Special Rept 2-SR-89-001:on 890422,limiting Condition for Operation Initiated Due to Two Inoperable Fire Barrier Penetration Seals in Common Augmented Offgas Bldg.On 890429, 7-day Time Frame Exceeded.Work Request Initiated BSEP-88-1228, Special Rept 1-SR-88-003:on 881120,7-day Time Frame for Limiting Condition for Operation Exceeded.Caused by Fire Door 211 Being out-of-svc to Prevent Wear & Possible Damage to Locking Seals & Interlocks1988-11-28028 November 1988 Special Rept 1-SR-88-003:on 881120,7-day Time Frame for Limiting Condition for Operation Exceeded.Caused by Fire Door 211 Being out-of-svc to Prevent Wear & Possible Damage to Locking Seals & Interlocks BSEP-88-0854, Special Rept 1-SR-88-001:limiting Condition for Operation (LCO) Established on 880405 for Fire Protection Deluge Valve 1-FP-DV-22 to Sprinkler Sys.Specified 14-day Time Frame of LCO Exceeded on 880419.Fire Watches Remain in Effect1988-09-0101 September 1988 Special Rept 1-SR-88-001:limiting Condition for Operation (LCO) Established on 880405 for Fire Protection Deluge Valve 1-FP-DV-22 to Sprinkler Sys.Specified 14-day Time Frame of LCO Exceeded on 880419.Fire Watches Remain in Effect BSEP-88-0850, Special Rept 2-SR-88-002:on 880119,unit Reactor Bldg Fire Detection Sys Zone 14 Instrumentation Declared Inoperable Due to Erroneous Fire Alarms.Limiting Condition for Operation Initiated.Sys Returned to Svc1988-09-0101 September 1988 Special Rept 2-SR-88-002:on 880119,unit Reactor Bldg Fire Detection Sys Zone 14 Instrumentation Declared Inoperable Due to Erroneous Fire Alarms.Limiting Condition for Operation Initiated.Sys Returned to Svc BSEP-88-0853, Followup Special Rept:On 871228,limiting Condition for Operation to Permit Fire Suppression Sprinkler Header from Svc Exceeded.Caused by Unavailability of Addl Flow Switch 2-FP-FS-4059 in Plant Supply Sys.Switch Repaired1988-09-0101 September 1988 Followup Special Rept:On 871228,limiting Condition for Operation to Permit Fire Suppression Sprinkler Header from Svc Exceeded.Caused by Unavailability of Addl Flow Switch 2-FP-FS-4059 in Plant Supply Sys.Switch Repaired BSEP-88-0625, Suppl to Special Rept:On 860307,two Designated Fire Barrier Limiting Conditions for Operation Initiated.Plant Mod Will Be Installed During Upcoming Refueling/Maint Outage to Resolve Subj Differential Pressure Problem1988-06-20020 June 1988 Suppl to Special Rept:On 860307,two Designated Fire Barrier Limiting Conditions for Operation Initiated.Plant Mod Will Be Installed During Upcoming Refueling/Maint Outage to Resolve Subj Differential Pressure Problem BSEP-88-0475, Special Rept 2-SR-88-004:on 880414,14 Day Time Frame Exceeded for Limiting Condition for Operations.Caused by Problems W/Acquisition of Replacement Parts.Repairs Made & Sprinkler Header Returned to Svc1988-05-13013 May 1988 Special Rept 2-SR-88-004:on 880414,14 Day Time Frame Exceeded for Limiting Condition for Operations.Caused by Problems W/Acquisition of Replacement Parts.Repairs Made & Sprinkler Header Returned to Svc BSEP-88-0474, Special Rept 1-SR-88-001:on 880419,14 Days Time Frame of Limiting Condition for Operation (LCO) Exceeded.Caused by Temporary Unavailability of Replacement Parts.Lco Will Remain in Effect Until Repairs Completed1988-05-11011 May 1988 Special Rept 1-SR-88-001:on 880419,14 Days Time Frame of Limiting Condition for Operation (LCO) Exceeded.Caused by Temporary Unavailability of Replacement Parts.Lco Will Remain in Effect Until Repairs Completed BSEP-88-0165, Special Rept:On 880119,reactor Bldg Fire Detection Sys Zone 14 Instrumentation Inoperable Due to Erroneous Fire Alarms.Caused Not Determined.Time Frame of 14 Days of Involved LCO Exceeded on 8802021988-03-0303 March 1988 Special Rept:On 880119,reactor Bldg Fire Detection Sys Zone 14 Instrumentation Inoperable Due to Erroneous Fire Alarms.Caused Not Determined.Time Frame of 14 Days of Involved LCO Exceeded on 880202 BSEP-88-0094, Special Rept 1-SR-88-002:on 880126,limiting Condition for Operation (LCO) Initiated for Fire Door 203 in Reactor Bldg to Permit Opening Door to Help Prevent Wear & Possible Damage to Locking Seals & Interlocks.Lco Exceeded on 8802021988-02-10010 February 1988 Special Rept 1-SR-88-002:on 880126,limiting Condition for Operation (LCO) Initiated for Fire Door 203 in Reactor Bldg to Permit Opening Door to Help Prevent Wear & Possible Damage to Locking Seals & Interlocks.Lco Exceeded on 880202 BSEP-88-0037, Special Rept 2-SR-88-001:on 880110,7-day Time Frame of Fire Barrier Limiting Condition for Operation for Fire Door 203 Exceeded.Fire Watches Established & Will Be Maintained During Remainder of Refueling/Maint Outage1988-01-19019 January 1988 Special Rept 2-SR-88-001:on 880110,7-day Time Frame of Fire Barrier Limiting Condition for Operation for Fire Door 203 Exceeded.Fire Watches Established & Will Be Maintained During Remainder of Refueling/Maint Outage BSEP-87-1095, Ro:On 870119,one of Four Fuel Loading Chambers Not in Location Where hands-on Inventory Could Be Performed at Site.Chamber Declared Loss Following Investigation.Chamber Was Probably Inadvertently Shipped to Burial Facility1987-09-25025 September 1987 Ro:On 870119,one of Four Fuel Loading Chambers Not in Location Where hands-on Inventory Could Be Performed at Site.Chamber Declared Loss Following Investigation.Chamber Was Probably Inadvertently Shipped to Burial Facility 1998-10-30 Category:TEXT-SAFETY REPORT MONTHYEARML20217N3271999-10-21021 October 1999
[Table view]Part 21 Rept Re non-linear Oxygen Readings with Two (2) Model 225 CMA-X Containment Monitoring Sys at Bsep.Caused by High Gain Produced by 10K Resistor Across Second Stage Amplifier.Engineering Drawings Will Be Revised BSEP-99-0168, Monthly Operating Repts for Sept 1999 for Bsep,Units 1 & 2. with1999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Bsep,Units 1 & 2. with ML20212D0431999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Brunswick Steam Electric Plant,Units 1 & 2 ML20210P9441999-08-10010 August 1999 Safety Evaluation Accepting Licensee Assessment of Impact on Operation of Plant,Unit 1,with Crack Indications of 2.11, 6.36 & 1.74 Inches in Three Separate Jet Pump Risers ML20210P9181999-08-10010 August 1999 Safety Evaluation Authorizing Request for Reliefs CIP-01,02, 06,07,08,09,10 & 11 (with Certain Exceptions) & 12-18,for Second 10-year ISI Interval.Request CIP-04 & 05 Would Result in hardship,CIP-03 Not Required & CIP-11 Denied in Part ML20210N2341999-08-0505 August 1999 SER Accepting Response to NRC GL 87-02, Verification of Seismic Adequacy of Mechanical & Electrical Equipment in Operating Reactors,Unresolved Safety Issues (USI) A-46 ML20210R1191999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Bsep,Units 1 & 2 ML20210R1311999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for Bsep,Unit 2 BSEP-99-0118, Monthly Operating Repts for June 1999 for Bsep,Units 1 & 2. with1999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Bsep,Units 1 & 2. with BSEP-99-0095, Monthly Operating Repts for May 1999 for Brunswick Steam Electric Plant,Units 1 & 2.With1999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Brunswick Steam Electric Plant,Units 1 & 2.With ML20210M8581999-05-14014 May 1999 B214R1 RPV Hydrotest Bolted Connection Corrective Action Evaluation, Rev 0 ML20211L3711999-05-10010 May 1999 Rev 0 to ESR 98-00333, Unit 2 Invessel Feedwater Sparger Evaluation ML20206G1871999-05-0404 May 1999 Safety Evaluation Approving Third 10-year ISI Program Requests for Relief (RR) RR-08,RR-15 & RR-17 BSEP-99-0075, Monthly Operating Repts for Apr 1999 for Brunswick Steam Electric Plant,Unit 1 & 2.With1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Brunswick Steam Electric Plant,Unit 1 & 2.With ML20206N1791999-04-23023 April 1999 Rev 0 to 2B21-0554, Brunswick Unit 2,Cycle 14 Colr BSEP-99-0059, Monthly Operating Repts for Mar 1999 for Brunswick Steam Electric Plant,Units 1 & 2.With1999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Brunswick Steam Electric Plant,Units 1 & 2.With ML20205F9031999-03-30030 March 1999 Safety Evaluation Supporting Proposed Rev to BSEP RERP to Licenses DPR-62 & DPR-71,respectively ML20206N1831999-02-28028 February 1999 Rev 0 to Suppl Reload Licensing Rept for Bsep,Unit 2 Reload 13 Cycle 14 BSEP-99-0043, Monthly Operating Repts for Feb 1999 for Brunswick Steam Electric Plant,Units 1 & 2.With1999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Brunswick Steam Electric Plant,Units 1 & 2.With ML20203D7061999-02-0909 February 1999 SER Accepting Proposed Alternatives Contained in Relief Requests PRR-04,VRR-04,VRR-13,PRR-01,PRR-03,VRR-01.VRR-07, VRR-08 & VRR-09 Denied BSEP-99-0005, Monthly Operating Repts for Dec 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With1998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With BSEP-98-0231, Monthly Operating Repts for Nov 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With1998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With BSEP-98-0218, Monthly Operating Repts for Oct 1998 for Bsep,Units 1 & 2. with1998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Bsep,Units 1 & 2. with BSEP-98-0210, Special Rept:On 980824,temp Element 2-CAC-TE-1258-22 Failed. Cause of Failed Temp Element Cannot Be Conclusively Determined.Temp Element Will Be Replaced & Cable Connections Repaired1998-10-30030 October 1998 Special Rept:On 980824,temp Element 2-CAC-TE-1258-22 Failed. Cause of Failed Temp Element Cannot Be Conclusively Determined.Temp Element Will Be Replaced & Cable Connections Repaired ML20154P8151998-10-16016 October 1998 SER Accepting Revised Safety Analysis of Operational Transient of 920117,for Plant,Unit 1 ML20154P8591998-10-16016 October 1998 SER Accepting Equivalent Margins Analysis for N-16A/B Instrument Nozzles for Plant,Units 1 & 2 BSEP-98-0202, Monthly Operating Repts for Sept 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With1998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With ML20151Y6211998-09-14014 September 1998 BSEP Rept Describing Changes,Tests & Experiments, for Bsep,Units 1 & 2 ML20151Y6371998-09-14014 September 1998 Changes to QA Program, for Bsep,Units 1 & 2 BSEP-98-0185, Monthly Operating Repts for Aug 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With1998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With ML20151T5021998-08-0505 August 1998 Project Implementation Plan, Ngg Yr 2000 Readiness Program, Rev 2 BSEP-98-0164, Monthly Operating Repts for July 1998 for BSEP Units 1 & 21998-07-31031 July 1998 Monthly Operating Repts for July 1998 for BSEP Units 1 & 2 ML20236T1961998-07-0101 July 1998 Rev 1 to 2B21-0088, Brunswick Unit 2,Cycle 13 Colr ML20236T1921998-07-0101 July 1998 Rev 1 to 1B21-0537, Brunswick Unit 1,Cycle 12 Colr BSEP-98-0142, Monthly Operating Repts for June 1998 for BSEP Units 1 & 21998-06-30030 June 1998 Monthly Operating Repts for June 1998 for BSEP Units 1 & 2 ML20236T1971998-06-30030 June 1998 Rev 2 to 24A5412, Supplemental Reload Licensing Rept for Brunswick Steam Electric Plant Unit 2 Reload 12 Cycle 13 ML20249B9691998-06-11011 June 1998 Rev 1 to VC44.F02, Brunswick Steam Electric Plant,Units 1 & 2,ECCS Suction Strainers Replacement Project,Nrc Bulletin 96-003 Final Rept BSEP-98-0129, Monthly Operating Repts for May 1998 for Bsep,Units 1 & 21998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Bsep,Units 1 & 2 ML20151S9041998-05-31031 May 1998 Revised Pages to Monthly Operating Rept for May 1998 for Brunswick Steam Electric Plant,Unit 1 BSEP-98-0104, Monthly Operating Repts for Apr 1998 for Brunswick Steam Electric Plant,Units 1 & 21998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Brunswick Steam Electric Plant,Units 1 & 2 ML20151S8991998-04-30030 April 1998 Revised Pages to Monthly Operating Rept for Apr 1998 for Brunswick Steam Electric Plant,Unit 1 ML20247N7501998-04-30030 April 1998 Rev 0 to BSEP Unit 1,Cycle 12 Colr ML20247N7721998-04-30030 April 1998 Rev 0 to J1103244SRLR, Supplemental Reload Licensing Rept for BSEP Unit 1,Reload 11,Cycle 12 ML20217K8461998-04-24024 April 1998 Safety Evaluation Approving Proposed Use of Code Case N-535 at Brunswick Unit 1 During Second 10-yr Interval,Pursuant to 10CFR50.55a(a)(3)(i).Authorizes Use of Code Case N-535 Until Code Case Included in Future Rev of RG 1.147 ML20217K3941998-04-24024 April 1998 SER Approving Relief Request for Pump Vibration Monitoring, Brunswick Steam Electric Plant,Units 1 & 2 ML20217E6841998-04-23023 April 1998 Safety Evaluation Accepting Code Case N-547, Alternative Exam Requirements for Pressure Retaining Bolting of CRD Housings ML20217E7471998-04-21021 April 1998 Safety Evaluation Accepting Alternative to Insp of Reactor Pressure Vessel Circumferential Welds ML20217B5241998-04-20020 April 1998 SE Accepting Licensee Request for Approval to Use Alternative Exam Requirement for Brunswick,Unit 1,reactor Vessel Stud & Bushing During Second 10-yr ISI Interval Per 10CFR50.55a(a)(3)(ii) BSEP-98-0080, Monthly Operating Repts for Mar 1998 for Bsep,Units 1 & 21998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Bsep,Units 1 & 2 ML20216B1041998-03-0404 March 1998 SER Approving Alternative to Insp of Reactor Pressure Vessel Circumferential Welds for Brunswick Steam Electric Plant, Unit 1 1999-09-30 |
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Carolina Power & Light Company - 1- 11 Brunswick Steam Electric-Plant' BI SEP 25' p'I *. 08 1
~P. 0.. Box-10429.
'Southport,'NC 28461_0429. ]?
September 22, 1987 '!
-i 0 . FILE: B09-13510C LSERIAL: BSEP/87-1079 Dr. .J. Nelson Grace, Administrator:
- U.S. Nuclear Regulatory Commission W
Suite 2900 !
101 Marietta Street NW- 't l
' Atlanta, GA' -30323 BRUNSWICK STEAM ELECTRIC PLANT UNIT 2 DOCKET NO. 50-324 LICENSE NO. DPR-62 SPECIAL' REPORT PER TECHNICAL SPECIFICATION 3.7.8 AND PURSUANT TO TECHNICAL SPECIFICATION 6.9.2 (2-SR-87-001).
Dear Dr. Grace:
On August 24, 1987, at 0430 hours0.00498 days <br />0.119 hours <br />7.109788e-4 weeks <br />1.63615e-4 months <br />, a Unit 2 fire barrier LCO was' initiate'd on penetration seal No. DG-1-096, fire door 003. This door, which'is located on the 1-foot 6-inch elevation of the Units 1 and 2 common diesel generators' four-day fuel oil storage rooms, provides personnel .ac~ cess :between rooms 2 ..
and 3. The LCO.was initiated to repair the door as it would not.close and latch properly. Discovery of.the door inoperability wasl.made'during performance of weekly Diesel Generator Building Swinging Fire Door-Inspection,-
Periodic Test (PT)-34.1.3.0. On August .31, '1987, at 0430 hours0.00498 days <br />0.119 hours <br />7.109788e-4 weeks <br />1.63615e-4 months <br />', the specified.' -
l seven-day time frame of the involved LCO.was exceeded. . Repairs to the subject-door were completed on August 31, 1987, and at 1500 hours0.0174 days <br />0.417 hours <br />0.00248 weeks <br />5.7075e-4 months <br />, the LCO was
[:
canceled and the door was returned to. service.
]
Very truly yours,-
Q. - -
C. R. Dietz,-General Manager j Brunswick. Steam. Electric Plant ij l
MJP/cj.
Lj Enclosure q cc: .NRC Document Control Desk .
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