3F1096-03, Monthly Operating Rept for Sept 1996 for Crystal River Unit 3

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Monthly Operating Rept for Sept 1996 for Crystal River Unit 3
ML20129B173
Person / Time
Site: Crystal River Duke Energy icon.png
Issue date: 09/30/1996
From: Dao T, Kelly L
FLORIDA POWER & LIGHT CO., FLORIDA POWER CORP.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
3F1096-03, 3F1096-3, NUDOCS 9610220348
Download: ML20129B173 (5)


Text

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Florida Power CORPORATON onuus no October 11, 1996 3F1096-03 U. S.' Nuclear Regulatory Commission Attn: Document Control Desk Washington, DC 20555-0001

Subject:

Monthly Operating Report

Dear Sir:

Attached is the Crystal River Unit-3 September 1996 Monthly Operating Report.

.This report is submitted in accordance with Technical Specification 5.7.1.2.

Sincer,ely, ALarry C. Kelley JC Director, Nuclear Operatio s Site Support LCK/ff Attachment xc: Regional Administrator, Region II Senior Resident Inspector NRR Project Manager

[ D Dbckohoo$002 l PDR CRYSTAL RVER ENERGY COMPLEX: 15700 W Power Une St . Crystal FWver, Florida 344284708 . (352) 7966486 A Fkwide Progress Company

' OPERATING DATA REPORT .

DOCKET NO. 50-302 UNIT FLCRP-3 DATE OCT 3,1996 COMPLETED BY T V Dao ;gd N4.Ov TELEPHONE (352)795-6486 (

OPERATING STATUS

1. ~ UNIT NAME:.. . .. ........ ... . . . . . . . . . . . . . . . . . . . . CRYSTAL RIVER UNIT 3
2. REPORTING PERIOD:..... . . . . . ... . . . . . . SEPTEMBER -
3. LICENSED THERMAL POWER (MWt):..... . ..... .. . .. 2544  !
4. NAMEPLATE RATING (GROSS MWe):.. .. . . .. . . 890
5. DESIGN ELECTRICAL RATING (NET MWe):.. . . .. . .. . 825
6. MAXIMUM DEPENDABLE CAPACITY (GROSS MWe):.. 860 7, MAXIMUM DEPENDABLE CAPACITY (NET MWe):.. . . 818
8. IF CHANGES OCCUR IN CAPACITY RATINGS (ITEMS NUMBER 3 THROUGH 7) SINCE LAST REPORT. GIVE REASONS: l l
9. POWER LEVEL TO WHICH RESTRICTED, IF ANY (NET MWe): N/A l
10. REASONS FOR RESTRICTIONS,IF ANY: N/A THIS MONTH YR. TO DATE CUMULATIVE
11. HOURS IN REPORTING PERIOD 720.0 6,575.0 171,407.0
12. NUMBER OF HOURS REACTOR WAS CRITICAL 66.0 ' 3.308.1 117.416.2
13. REACTOR RESERVE SHUTDOWN HOURS 0.0 0.0 1.280.6
14. HRS GENERATOR ON LINE 45.0 3.109.5 115.328.7
15. UNIT RESERVE SHUTDOWN HOURS 0.0 0.0 . 0.0
16. GROSS THERMAL ENERGY GENERATED (MWH) 119.146 7.465,052 268.847.210
17. GROSS ELECTRICAL ENERGY GENERATED (MWH) 34.734 2.547,840 91,894.033 -
18. NET ELECTRICAL ENERGY GENERATED (MWH) 32,771 2.417,371 87,402.384-l 19. UNIT SERVICE FACTOR 6.3% 47.3 % 67.3 %

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20. UNIT AVAILABLE FACTOR 6.3% 47.3 % 67.3 %
21. UNIT CAPACITY FACTOR (using MDC net) 5.6% 44.9 % 63.1 %
22. UNIT CAPACITY FACTOR (using DER net) 5.5% 44.6 % 61.8 %

l 23. UNIT FORCED OUTAGE RATE 93.8 % 28.8 % 1F ]

'94 SHUTDOWNS SCHEDULED OVER NEXT SIX MONTHS (TYPE, DATE AND DURATION OF EACH):

85. IF SHUTDOWN AT END OF REPORT PERIOD. ESTIMATED DATE OF STARTUP:
36. UNITS IN TEST STATUS (PRIOR TO COMMERCIAL OPERATION):

THIS ITEM IS NOT APPLICABLE TO CR-3 FORECAST ACHIEVED INITIAL CRITICALITY NA NA INITIAL ELECTRICITY NA NA COMMERCIAL OPERATION NA NA

'6.

AVERAGE DAILY UNIT POWER LEVEL DOCKET NO. 50-302 f UNIT FLCRP-3 DATE _OCT 3.1996 COMPLETED BY T V Dao TELEPHONE (352) 795-6486 MONTH SEPTEMBER DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net) (MWe-Net) .

1 787 17 0 2 579 18 0 3 0 19 0-4 0 20 0 5 0 21 0 6 0 22 0 7 0 23 0 8 0 24 0 9 0 25 0 l

10 0 26 0 11 0 27 _ 0 12 0 28 0 ,

13 , 0 29 0 14 0 30 0 15 0 31 N/A _

16 0 INSTRUCTIONS:

On this format, list the daily average unit power level in MWe-Net for each day in the reporting month. Compute to the nearest whole megawatt.

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.- e UNIT SHUTDOWNS AND POWER REDUCTIONS ,

DOCKET NO. 50-302 UN(T ~ FLCRP-3 ,

REPORT MONTH. SEPTBMER DATE OCT 3.1996 COMPLETED BY T V Dao e TELEPHONE (352)795-s4ee e

NO. DATE - TYPE (1) DURATION FEASON (2) METHOO OF UCENSEE SYSTEM COMPONENT CAUSE AND CORRECTIVE ,

HOURS SHUTTING EVENT CODE (4) CODE (5) ACTION TO PREVENT DOWN REACTOR (3) REPORT # RECURRENCE 96-24 960902 F 0 A 5 N/A HA VALVEX Power reduction to take the main turbine off line to troubleshoot and repair low lube oil pressure.

W 25 960902 F 289.2 A 1 N/A HA VALVEX The unit was off line to replace a cracked pipe in the main turbine tube oil tank.

96-26 960914 F 385.8 D 4 5 020-00 EE ENGINE Reactor remained in cold shutdown to resolve design issue related to emergency diesel maximum electricalloading.

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1 2 3 4 5 j F: FOHCED NASON: METHOD EXHIBIT G - 94STRX:TIONS EXHIBIT I- SAME SOURCE S. SCHEDULED A-EQUIPMENT FAILUN 1-MANUAL FOR PNPARATION OF DATA B-MAMTENANCE OR TEST 2-MAprJAL SCRAM ENTRY SHEETS FOR LICENSEE C-REFUELING 3-AUTO SCRAM EVENT REPORT (LEFQ FLE D-NGULATORY l ESTRICTION N (NUREG-0161)

E-OPERATORTRAINING & 6-REDUCED LOAD LICENSE ADMINISTRATION 0-OTHER F-ADEPHISTRATION G-OPERATIONAL ERROR (EXPLAM) tv-0THER

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MONTHLY OPERATIONAL

SUMMARY

STATEMENT l

DOCKET NO. 50-302 UNIT FLCRP-3 DATE OCT 3,1996 COMPLETED BY T V Dao TELEPHONE (352)795-6486 MONTH: SEPTEMBER

SUMMARY

STATEMENT:

Crystal River Unit 3 came off line on 09/02 to troubleshoot and repair decreasing tube oil pressure to the main turbine. The repair was cornpleted on 09/14. The unit remained in cold shutdown through the remainder of September to resolve the emergency diesel generator maximum electrical loading issue.

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