3F0796-01, Monthly Operating Rept for June 1996 for Crystal River Unit 3

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Monthly Operating Rept for June 1996 for Crystal River Unit 3
ML20115H417
Person / Time
Site: Crystal River Duke Energy icon.png
Issue date: 06/30/1996
From: Boldt G, Dao T, Terry J
FLORIDA POWER CORP.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
3F0796-01, 3F796-1, NUDOCS 9607230113
Download: ML20115H417 (5)


Text

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Florida Power CORPORATION l

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l July 12,1996 l 3F0796-01 l U. S. Nuclear Regulatory Commission ,

Attn: Document Control Desk i Washington, DC 20555-0001 '

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Subject:

Monthly Operating Report

Dear Sir:

Attached is the Crystal River Unit-3 June 1996 Monthly Operating Report. This report is submitted in accordance with Technical Specification 5.7.1.2. i Sincerely, kW G. L. oldt Vice President Nuclear Operations GLB/ff Attachment xc: NRR Project Manager Regional Administrator, Region II Senior Resident Inspector g 9607230113 960630 PDR ADOCK 05000302

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R PDR CRYSTAL FWER ENEH3Y COMPLEX: 15760 W Power une St . Crystal River, Floride 344284708 . (352) 795 6486 A Fkwida Progress Corupany ,

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OPERATING DATA REPORT DOCKET NO. 50-302 UNIT FLCRP-3 l

DATE JULY 3,1996 l

COMPLETED BY T V Dao jkUM TELEPHONE (352) 795-6486 I i OPERATING STATUS 1

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1. UNIT N AME:..... . .. . . ........ .. . CRYSTAL RIVER UNIT 3 -
2. REPORTING PERIOD:.. . . . . . . . . JUNE
3. LICENSED THERMAL POWER (MWt):. . . . . .. 2544 l
4. NAMEPLATE RATING (GROSS MWe):. . . . . . 890
5. DESIGN ELECTRICAL RATING (NET MWe):. . . . . . 825
6. MAXIMUM DEPENDABLE CAPACITY (GROSS MWe):. 860
7. MAXIMUM DEPENDABLE CAPACITY (NET MWe):. . 818
8. IF CHANGES OCCUR IN CAPACITY RATINGS (ITEMS NUMBER S THROUGH 7) SINCE LAST REPORT, GIVE REASONS:
9. POWER LEVEL TO WHICH RESTRICTED,IF ANY (NET MWe): N/A
10. REASONS FOR RESTRICTIONS,IF ANY: N/A THIS MONTH YR. TO DATE CUMULATIVE
11. HOURS IN REPORTING PERIOD 720.0 4,367.0 169,199.0
12. NUMBER OF HOURS REACTOR WAS CRITICAL 670.8 1,754.1 115.862.2
13. REACTOR RESERVE SHUTDOWN HOURS 0.0 0.0' 1,280.6
14. HRS GENERATOR ON LINE 585.6 1,576.5 113,795.7 .
15. UNIT RESERVE SHUTDOWN HOURS 0.0 0.0 0.0
16. GROSS THERMAL ENERGY GENERATED (MWH) 1,374.742 3,697,796- 265.079.954 l
17. GROSS ELECTRICAL ENERGY GENERATED (MWH) 463.552 1,249.931' ' 90.596.124 l
18. NET ELECTRICAL ENERGY GENERATED (MWH) 439,198 1.186,280 86,171,293 l
19. UNIT SERVICE FACTOR 81.'3% 36.1 % 67.3 % )
20. UNIT AVAILABLE FACTOR 81.3 % 36.1 % 67.3 % i
21. UNIT CAPACITY FACTOR (using MDC net) 74.6 % 33.2 % 63.0 %
22. UNIT CAPACITY FACTOR (using DER net) 73.9 % 32.9 % 61.7 %
23. UNIT FORCED OUTAGE RATE 18.7% 27.0 % 15.4 %
24. SHUTDOWNS SCHEDULED OVER NEXT SIX MONTHS (TYPE, DATE, AND DURATION OF EACH):
25. IF SHUTDOWN AT END OF REPORT PERIOD. ESTIMATED DATE OF STARIUP:
26. UNITS IN TEST STATUS (PRIOR TO COMMERCIAL OPERATION):

THIS ITEM IS NOT APPLICABLE TO CR-3 FORECAST ACHIEVED INITIAL CRmCALITY NA NA l INITIAL ELECTRICITY NA NA ]

COMMERCIAL OPERATION NA NA 'I l

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, AVERAGE DAILY UNIT POWER LEVEL DOCKET NO. 50-302 UNIT FLCRP-3 DATE JULY 3,1996 COMPLETED BY T V Dao TELEPHONE (352)795-6486 MONTH JUNE DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net) (MWe-Net) i 1 0 17 '847 2 0 18 847 3 0 19 846 4 0 20 845 5 0 21 845 6 42 22 819.

7 184 23 651 8 490- 24 714 9 845 25 840 10 723 26 839 11 705' 27 _ 840 12 704 28 _ 843 13 -699 29 845 14 803 30 846 15 844 31 N/A-16 -846 INSTRUCTIONS:

l On this format, list the daily average unit power level in MWe-Net for each day in the l reporting month, Compute to the nearest whole megawatt.

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UNIT SHUTDOWNS AND POWER REDUCTIONS ,

DOCKET NO. 5o-3o2 ,

UNIT FLCRP-3 ,

REPORT MONTH JUNE DATE JULY 3.1996 COMPLETED BY T V Dao TELEPHONE (352) 795-6486 NO. DATE TYPE (1) DURA 110N REASON (2) METHOD OF UCENSEE SYSTEM COMPONENT CAUSE AND CORRECTIVE HOURS SHUTTING EVENT CODE (4) CODE (5) ACTION TO PREVENT DOWN REACTOR (3) REPORT # RECURRENCE 96-14 960601 F 134.4 B 4 N/A HA VALVEX Continuation of the turbine EHC oil outage.

96-15 960606 S 0 A 5 N/A ZZ 777777 Power escalation and condenser air leak repair.

96-16 960610 S 0 A 5 N/A HF PIPEXX Power reduction to repair circulating water purnp CWP-1D discharge header through wal!

leaks.

96-17 960622 S 0 A 5 N/A HF 777777 Power reduction to repair a loose debris filter flap in the "B' waterbox and a through wall leak in the adjacent fiberglass piping.

1 2 3 4 5 F: F0 FACED NASON. METHOD EXHIBIT G -INSTRUCTONS EXHIBfT I- SAME SOURCE S: SCHEDULED A-EQUIPMENT FAILUN 1-MANUAL FOR PREPARATION OF DATA EMAAINTENANCE OR TEST 2-MANUAL SCRAM ENTRY SHEETS FOR LICENSEE C-REFUELING 3-AUTO SCRAM EVENT REPORT (LER) FILE D-REGULATORY RESTIMCTION 4-CONTINUED (NUREG-0181)

E-OPERATORTRAINING & 5-REDUCED LOAD LICENSE ADMINISTRATION 9-OTHER F-ADMINISTRATION G-OPERATIONAL ERROR (EXPLAIN)

M-0THER

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, MONTHLY OPERATIONAL

SUMMARY

STATEMENT I

DOCKET NO. 50-302 l UNIT FLCRP-3 DATE JULY 3,1996 COMPLETED BY T V Dao TELEPHONE (352)795-6486 MONTH: JUNE I

SUMMARY

STATEMENT:

Crystal River Unit 3 went on line on 06/06 following the turbine I EHC oil outage. j l

Three other power reductions occurred during this period. l Power escalation was delayed on 06/06 to troubleshoot and repair a condenser air leak. Power was reduced on 06/10 to repair through wall leaks in the circulating water pump CWP-1D discharge header.

Power was reduced on 06/22 to repair a loose debris filter flap in the "B" waterbox and a through wallleak in the adjacent fiberglass piping, i

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