ML20135A468
ML20135A468 | |
Person / Time | |
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Site: | River Bend |
Issue date: | 02/20/1997 |
From: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV) |
To: | |
Shared Package | |
ML20135A456 | List: |
References | |
50-458-96-17, NUDOCS 9702270189 | |
Download: ML20135A468 (24) | |
See also: IR 05000458/1996017
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ENCLOSURE 2
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U.S. NUCLEAR REGULATORY COMMISSION
REGION IV
Docket No.: 50-458 ;
License No.: NPF-47 ;
Report No.: 50-458/96-17 _
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Licensee: Entergy Operations, Inc.
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' Facility: River Bend Station :
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Location: 5485 U.S. Highway 61
St. Francisville, Louisiana 70775 - i
Dates: December 15,1996 through February 1,1997
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Inspectors: W. F. Smith, Senior Resident inspector
D. L. Proulx, Resident inspector j
G. M. Good, Senior Emergency Preparedness Analyst, ;
Division of Reactor Safety
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Approved By: P. H. Harrell, Chief, Project D -
Division of Reactor Projects !
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Attachment: Supplemental information
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9702270139 970220
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PDR ADOCK050004y8
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EXECUTIVE SUMMARY I
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River Bend Station l
NRC Inspection Report 50-458/96-17
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This inspection included aspects of licensee operations, maintenance, engineering, and !
plant suppcet. The report covers a 7-week period of resident inspection. I
Operations
In general, operator performance was good during this inspection period. Control
room activities were carried out in a business-like manner, with good
communications observed by the inspectors. Decisions made in support of !'
maintenance were usually conservative.
The reduction in power in support of balance-of-plant repairs was completed
without incident, as were the control rod scram testing and mairi steam isolation
valve cycling activities (Section 01.1).
The licensee responded well to the cold weather advisories warning the River Bend
area of snow on December 18,1996. Operations developed a contingency watch
bill and the Emergency Planning organization interfaced with external authorities to
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ensure emergency evacuation routes would i,e kept open (Section 01.2). l
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- Continued configuration control problems were noted when an operator identified
i the control switches were in the OFF position for both of the Division 111 emergency
l diesel generator (EDG) starting air compressors. Though nonsafety related, the
compressors were important in that they maintained pressure in the safety-related
air receivers. Although the licensee was unable to determine the cause, the
licensee implemented good corrective actions and responded appropriately to the
issue of configuration controls (Section 02.1).
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- Equipment was properly staged for two emergency operating procedure (EOP) ;
supporting enclosures. In addition, the on-shift operators demonstrated good I
knowledge to perform these procedures (Section 03.1).
l Maintenance
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- The licensee's response to the f ailure of Rod Control and Information System
l (RC&lS) Power Supply C11-PS1 demonstrated good teamwork, management
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oversight, quality assurance, and proper utilization of the licensee's administrative
controls over maintenance work and plant design configuration (Section M1.1).
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- The replacement of the standby service water (SSW) loop seal valves was
performed in a step-by-step manner and in accordance with procedures. Good
coordination was observed between operations and maintenance pes.m:! ;n
establishing conditions for the work, including a freeze seal (Section M1.2).
- Af ter repeated f ailures of the containment airlock door seal air ball valves, the
licensee appropriately formed a Significant Event Review Team (SERT) to determine
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the root causes and recommend permanent corrective action. Actions already
implemented, as well as those recommended, appeared to be appropriate to correct
the problem. Mechanics effectively performed the work and postmaintenance
testing (Section M1.3).
The licensee identified a fGilure to implement a Technical Specification (TS)
surveillance requirement (SR), which required monthly verification that the hydrogen
mixing valves were closed. The licensee made an error in renumbering requirements
for the Improved TS, which resulted in an incorrect procedure being referenced in
the TS/ surveillance procedure cross-reference matrix. The licensee's corrective
actions were satisf actory to prevent recurrence. A noncited violation (NCV) was
identified for failure to perform the TS surveillance at the correct frequency
(Section M1.4).
A procedure upgrade reviewer demonstrated excellent performance in identifying
and documenting on a condition report (CR) a missed surveillance requirement
associated with the control rod scram accumulator instrumentation testing. An
NCV was identified for f ailure to maintain the technical adequacy of the surveillance
test procedure implementing the requirement to test the common control room
alarm from each of the 145 scram accumulators (Section M1.5).
- The inspectors identified a violation for failure to follow instructions that were
instituted to preclude dropping items into the SSW cooling tower basin. The
inservice testing (IST) of the Division ll SSW pumps was otherwise performed
properly and in accordance with the procedure (Section M1.6).
- The surveillance test on the low pressure coolant injection (LPCI) Pump C start logic
was performed properly and in accordance with procedures. Technicians employed
good self-checking and sound electrical safety practices while performing this test
(Section M1.7).
Enaineerina
- Design Engineering demonstrated a good questioning attitude in reviewing the 1990
licensee response to NRC Information Notice 88-76, Recent Discovery of a
Phenomenon not Previously Considered in the Design of Secondary Containment
Pressure Control relative to possible secondary containment positive pressures
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caused by low outside temperature extremes, immediate action to provide the !
operators with outside temperature dependent acceptance criteria for secondary I
containment pressure was appropriate to the circumstances pending implementation l
of permanent corrective action (Section E2.1).
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Plant Support
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Housekeeping in *a plant continued to be excellent. It was noteworthy that the
l construction area in which the new alternate decay heat removal system was being
installed was being maintained clean and orderly (Section 01.1).
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The commitment to perform on-shift dose assessments was appropriately described
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in the licensee's emergency plan and implementing procedures. Further evaluation
of the information obtained using Temporary Instruction (TI) 2515/134 will be
conducted by NRC Headquarters personnel (Section P3.1).
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REPORT DETAILS
Summarv of Plant Status
The plant operated at essentially 100 percent power for the duration of this inspection
period, except on January 18 through January 21,1997, when power was reduced to
approximately 60 percent in support of balance-of-plant maintenance and reactor control
rod repositioning.
1. Operations
01 Conduct of Operations
, 01.1 General Comments (71707)
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The inspectors conducted frequent reviews of ongoing plant operations including
f control room observations, attendance at plan-of-the-day meetings, and plant tours.
l In general, the conduct of plant operators was professional and reflected a focus on
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safety. Decisions made in support of maintenance were usually conservative based
on the inspectors' routine reviews of TS limiting conditions for operation (LCO)
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entered and exited. During plant tours, the inspectors found that housekeeping
continued to be excellent. Any minor discrepancies identified b" *.he inspectors
were promptly corrected. During several tours, the inspectors considered it
noteworthy that construction workers installing the new alternate decay heat ,
removal systems kept the areas orderly and clean. )
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The inspectors reviewed the operator actions to reduce power to 60 percent on i
January 18, in support of corrective maintenance on the nonsafety-related isophase l
bus duct cooling fan, which reduced the heat load on the isophase duct to a level
that would not cause overheating without the fan.
The operators followed the appropriate operating procedures to reduce power and
then subsequently restored power in a well-controlled manner. The licensee also i
utilized the lower plant power level to replace a shaft seal on a heater drain pump, l
replace a relief valve on a feedwater pump gear increaser, perform scram time
testing of five control rod hydraulic control units that were overhauled, and full-
stroke cycle the main steam isolation valves. Testing and repairs were successfully
accomplished without incident.
01.2 Licensee Actions in Response to Snow Warninas (71707)
On December 18,1996, the National Weather Service placed the St. Francisville
area, in a snow warning. The inspectors evaluated the contingency plans that were
l implemented in the event emergency response became necessary. Operations !
! management published a shift coverage contingency plan that utilized qualified j
! personnel who resided close to the plant. Cold weather precautions had previously j
! been implemented. These actions were reviewed by the inspectors and were found j
! to be appropriate. Emergency Planning management interfaced with the Louisiana l
l Radiation Protection Division and confirmed that provisions were made through the
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Office of Emergency Preparedness and Federal Emergency Management Agency,
~ Region 6, to ensure that evacuation routes would remain open. }
The inspectors considered the preparations in response to the snow warning was l
appropriate to the circumstances. The forecasted snow did not arrive. i
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O2 Operational Status of Facilities and Equipment
O2.1 Additional Confiouration Control Deficiencies 9
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a. Lnjiipection
n Scope (71707) ;
The inspectors evaluated the response to CR 96-1923, where an operator identified
continuing problems with s"/ stem configuration controls. i
b. Observations and Findinas
NRC Inspection Report 50458/96-15 cited four examples of failure of the licensee !
to maintain configuration control of safety-related system valves and switches.
While in the process of implementing corrective actions focused on addressing the
apparent adverse trend in operations human performance, another problem was
identified by the licensee.
On November 8,1996, while perforraing the EDG building rounds, an operator
discovered the control switches for both starting air compressors for the Division Ill. I
EDG were in the OFF position. One of the two air tanks had dropped to 217 psig,-
which was below the pressure at which the compressor automatically starts. The
setpoint was approximately 225 psig. The operator informed the control room
promptly, placed the switches in the required auto position, and then initiated
CR 96-1923. The operations shift superintendent ordered a complete control board
lineup check on all three EDGs and no additional deficiencies were found. The
Division lli EDG was operable because air tank pressure did not decrease below the
160 psig minimum specified in the applicable TS.
The inspectors were concerned that although the compressors were not safety-
related equipment, the compressors had the important function of maintaining the
EDG starting air tanks at the required pressure. The licensee responded to the issue
by implementing a thorough investigation to determine the cause. Security
computer history was utilized to determine who was in the EDG building for the
time period it tould have taken for the air pressure to decay off. Each individual
was questioned, but none recalled leaving the switches in the OFF position. After
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about 2 months of investigation, the licensee concluded that the cause of the
l switches being out of the required position was indeterminate. The licensee did
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identify that, the operators sometimes turned off the compressors when checking
j the oil each shif t, especially when the tank pressure was near the setpoint for the
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compressors to start. The licensee theorized that an operator did that and forgot to l
l* restore the switches to the AUTO position.
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The licensee has since _ implemented many corrective action items as listed in the
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docketed reply to the Notice of Violation, dated January 24,1997. This issue was l
not cited as a violation because corrective actions were in the process of being' ]
implemented when this problem was identified.
l To avoid further violations, the licensee established a plant configuration control
l team, with the support of River Bend management, to maintain an aggressive
approach to monitor, track, and resolve configuration controlissues until j
performance is improved. The team leader and plant management have met with j
the inspectors on a periodic basis to keep the inspectors appraised of progress in
this area.
c. Conclusiong
l The inspectors concluded that th<s licensee is implementing good corrective actions
and has responded appropriately to the configuration control issues. The inspectors
l will evaluate the effectiveness of the licensee's actions during the followup
l inspections for closure of the violation in NRC Inspection Report 50-458/96-015.
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l 03 Operations Procedures and Documentation (71707)
O3.1 Walkdown of Enclosures for EOPs
On December <26 and 27,1996, the inspectors performed reviews of the licensee's
implementation of two enclosures for EOPs to verify the ' actions specified could be
performed. These support procedures were contained within Procedure EOP-5,
" Emergency Operating Procedures-Enclosures," Revision 9. The inspectors walked
down Enclosures 1 and 12, which addressed defeating the main turbine trip from
initiation of the reactor core isolation cooling system and injection into the reactor i
vessel with the condensate transfer system. The inspectors verified that all keys I
and tools were staged and that on-shift licensed operators were sufficiently familiar
with the actions stated in these enclosures. The inspectors concluded that the !
L licensee adequately trained the operators and staged materials for effective
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implementation of Enclosures 1 and 12 of Procedure EOP-5.
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08 Miscellaneous Operations issues (92901)
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08.1 Survey of TS Interoretations
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l The inspectors conducted a survey of the licensee's TS interpretations and j
l determined that no documents existed with informal references to NRC review and j
i- approval without formal NRC documentation. The inspectors emphasized to the
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licensee, at the exit interview, that any informal reference to NRC review and
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approvalin a TS interpretation is not recognized by the Commission and is not an l
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11. Maintenance
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M1 Conduct of Maintenance
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M 1.1 Replacement of Failed RC&lS Power Supolv
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a. Inspection Scope (62707.37551)
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The inspectors observed the licensee's actions in response to a failed RC&lS power . l
, supply that placed the plant in a condition where the TS required the plant to be ;
L shut down in 13 hours1.50463e-4 days <br />0.00361 hours <br />2.149471e-5 weeks <br />4.9465e-6 months <br /> if not corrected. ,
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b. Observations and Findinas
On January 8,1997, at 4:30 a.m., while the plant was operating at 100 percent !
power, the RC&lS inoperable alarm annunciated in the control room and could not '
l- be reset. Without this system being functional, the control rod withdrawallimiter '
l was inoperable, which prevented control rod withdrawal or insertion by normal
means, in addition, the control rod scram accumulator leakage and low pressure i
alarm function was disabled for all 145 control rods. The operators appropriately ,
entered Technical Requirements Manual Limiting Condition for Operation !
l (TLCO) 3.1.5.1, which required the operators to immediately declare the scram
l- accumulators inoperable. This action led the operators to TS 3.1.5.B, which
! required the operators to declare the associated control rods inoperable within 1
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At 5:30 a.m., the operators declared the control rods inoperable, which further led
l the operators to TS 3.1.3.E, which required the operators to shut down the reactor
and place the plant in Mode 3 (Hot Shutdown)in 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />, in addition, because
the rod withdrawallimiter was inoperable, TS 3.3.2.1 prohibited any control rod
movement except to scram. This meant that power could only be reduced to
approximately 70 percent by reactor flow reduction, and then the plant would be
shut down by a reactor scram from that power level to achieve Mode 3 conditions,
i The operators assembled the appropriate maintenance and engineering support and
! promptly informed licensee management of the problem and the potential plant
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transient. To better ensure control rod scram capability, the operators increased
monitoring of control rod scram accumulator pressures from once per week to every
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4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />. By approximately 8:30 a.m., the licensee had determined by
i. troubleshooting that RC&lS Power Supply C11-PS1 had failed. A new power
- supply was obtained from the plant warehouse and the failed ' power supply was
, removed from the panel. By this time, the licensee developed several contingency
i plans. A change to TLCO 3.1.5.1 was being considered, which would have allowed
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monitoring the scram accumulator pressure and leakage alarm parameters instead of
declaring the accumulators inoperable. A backup power supply was sent in from ;
another nuclear facility, a temporary alteration waa being considered to enable the ;
accumulator alarms, and work was proceeding to install the new power supply in i
accordance with Maintenance Action item (MAI) 309925. However, the {
maintenance technicians discovered that two of the four mounting bracket screw
holes did not line up with the new power supply, which caused CR 97-0015 to be l
initiated.
The engineers supporting the work decided to repair the mounting bracket by drilling
new holes. They noted that another installed RC&lS Power Supply (C11-PS2) had a !
bracket that was similarly modified to accommodate a previous power supply i
replacement. At this point, maintenance personnel converted the Reference MAI to
a Compliance mal in accordance with administrative procedures because. a repair
was involved, which necessitated explicit documentation and instructions The
Reference MAI was only appropriate for exact replacements using skil' of the craft
and referencing the applicable drawings and standards. The inspeuors reviewed ,
the MAI package and found it to be in order and appropriate to the circumstances. l
In order to expedite restoration of RC&lS ability to function, Engineering personnel
issued an interim disposition of the CR to allow installation of the new power supply
with the modified mounting bracket. The inspectors reviewed the technical
justification for the disposition and found that it had sufficient basis. The inspectors
observed installation of the new power supply at approximately 12 noon and the ,
RC&lS became fully operational as the postmaintenance test was completed l
satisf actorily. At 1:19 p.m., the Facility Review Committee completed review and
approval of the CR disposition to modify the power supply mounting bracket. The
approved documentation included a 10 CFR 50.59 safety evaluation screening,
which appropriately did not require a safety evaluation.
On January 11, another RC&lS inoperable alarm annunciated in the control room.
The power supply was checked and found to be satisf actory. In about 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />, the
operators were able to reset the system and the cause was assumed to have been a
spurious signal from an individual hydraulic control unit transponder card. The
operators were instructed that should another alarm occur, to not attempt to reset
RC&lS until Engineering personnel analyzed the RC&lS panel diagnostic display.
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The licensee promptly revised TLCO 3.1.5.1 such that when the RC&lS became
inoperable, which disabled the hydraulic control unit accumulator alarms, the
l operators would no longer be required to declare the accumulators inoperable. The
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revised TLCO required verification of the affected accumulator pressure at equal or
greater than 1520 psig every 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />, and verify the affected accumulator water
drained every 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br />. This change was appropriately made pursuant to
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On January 20 and 21, additional RC&lS alarms occurred and as a result of l'
troubleshooting, the licensee determined that there was a broken multiple contact
plug 5 the RC&lS panel, which caused one of the connections to place intermittent '
noise on the signal. Also, while checking power supplies, the technicians found
alternating current noise on.the output of one of the power supplies and it was I
replaced. The licensee replaced the broken plug and the RC&lS was restored to i
operability. The system operated satisfactorily through the end of this inspection I
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The inspectors questioned what actions were to be taken to better ensure the
reliability of all 14 RC&lS power supplies. The licensee responded that closer i
monitoring of the power supply output voltage and noise would be incorporated into i
the preventive maintenance program for this system. i
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Throughout this maintenance activity, the inspectors observed good teamwork in an l
effort to minimize outage time, balanced with establishing sound technical bases for !
the engineering decisions made. Continuous management oversight and quality I
assurance inspections were provided. The quality assurance inspector j
demonstrated a good questioning attitude and ensured that the work'was properly )
done. j
c. Conclusions
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The inspectors concluded that the licensee's response to the failure of RC&lS Power
Supply C11-PS1 demonstrated good teamwork, good management oversight, and )
proper utilization of the licensee's administrative controls over maintenance work
and plant design configuration.
M1.2 Replacement of SSW Looo Seal Valves
a. Insoection Scope (62707)
On January 16,1997, the inspectors observed the performance of MAI 224396,
which replaced SSW Valves SWP-V656 and -V657. In addition, the inspectors
observed the applicatir'n of a freeze sealin accordance with Corrective Maintenance 1
Procedure CMP-9186, " Freeze Seals," Revision 8C. I
b. Observations and Findinas !
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The inspectors noted that the maintenance mechanics methodically established the ;
freeze seal in accordance with the procedure and implemented all applicable !
precautions. The licensee had previously exhibited weaknesses in the freeze sealing
process; therefore, the licensee's performance was noted to have been improved. 1
The inspectors noted that, except for minor administrative documentation errors j
that were immediately corrected, the task was performed properly and in i
accordance with the mal. Good coordination was observed between operations
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and maintenance personnel in establishing the freeze seal and draining the
associated piping.
c. Conclusions
The replacement of the SSW loop seal valves was performed in a step by-step
manner and in accordance with procedures. Good coordination was observed
between operations and maintenance personnelin establishing conditions for the
work.
M1.3 Repeated Failures of Containment Airlock Door Sealina Systems
a. Insoection Scope (62707.61726)
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On January 17,1997, the inspectors observed portions of the replacement of a
broken valve stem on the 171-foot elevation containment air lock inner door, upper
sealing system ball valve, in accordance with MAI 310118. The inspectors also
observed portions of the postmaintenance testing and reviewed the completed test
data.
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b. Observations and Findinas
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The inspectors found that the mal instructions were of sufficient detail for the skill ,
of the craf ts such that the quality of this maintenance activity was sufficiently l
controlled. The appropriate personnel and safety precautions were taken. The !
clearance was found to be appropriate and the work area on the floor grating was l
covered with mats to help prevent losses of tools and parts into the suppression
pool. Craft supervision was present during some of the work and provided
appropriate oversight. The craftsmen appeared adequately trained and experienced
and performed their work in a professional manner in accordance with the MAI
instructions. The postmaintenance air drop tests were performed in an excellent
manner. The test performers followed the procedure and exercised great care in
establishing a stable initial pressure to obtain meaningful results. Completed test
data was legible and calculations were correct.
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This was the second failure of a containment airlock door sealing system ball valve
stem. On December 26,1996, the lower ball valve in the same airlock door failed.
The licensee replaced the stem and subsequently determined that the stem seal o-
ring groove had signs of chloride stress corrosion cracking. This weakened the type
316 stainless steel stem and it eventually f ailed while in service from apparent
fatigue.
The containment airlock door seal system ball valves had a history of leakage
problems over the past year. To ensure the systems were maintained leak tight, the
licensee iricreased the frequency of the air drop surveillance test from the TS-
required periodicity of 18 months to quarterly. The licensee experienced several
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test failures during the past year. The licensee replaced ball valve Tefzel seats and
i air lanced the carbon steel accumulators to remove the rust particles that appeared
j to have caused scratches on the balls resulting in seating failures. The licensee
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removed the lubricant from the ball valves because the lubricant appeared to trap
the rust particles in the seating areas, in addition, the licensee concluded, in
- December 1996, that the valve body fasteners were not installed with sufficient i
i torque, thereby defeating the seat design. Successful drop tests following the l
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removal of lubricant and applying greater torque to the valve body fasteners led the
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licensee to believe they had solved the problem. However, tightening of the body '
i' and removing lubricant in combination with the presence of stress corrosion '
i cracking may have contributed to valve stem failure.
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The General Manager, Plant Operations directed a SERT be formed on January 21,
1997, to determine the root causes of the multiple failures of the air lock door
sealing systems and to implement permanent corrective actions. By January 24,
the SERT performed and implemented, in part, the following immediate corrective
actions:
Inspected ball valve balls and seats and replaced them if there were signs of
wear or scoring.
Replaced all of the Type 316 stainless steel ball valve stems with Type 630 ;
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stems, which were stronger and less vulnerable to chlorides.
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- Applied a light film of vendor-approved lubricant in the ball valves.
- Retorqued the ball valve body bolts to the greater torque.
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Air lanced the accumulator tanks to remove as much rust as possible.
Replaced the ball valve operating gear clamp pieces with new clamp pieces
with a thickness equal to the gear to ensure even forces on the valve stems.
The original clemp pieces were thinner than the gear, but were within -
drawing tolerances.
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- Removed all locking compound from the valves and fasteners. This
compound was four:d to be a potential source of chlorides which could lead
to stress corrosion cracking on stainless steel parts.
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The SERT was continuing its investigation as of tho end of this inspection period i
and has recomrnended a list of 31 action items, some of which were completed.
The SERT was considering design improvements that would eliminate the identified
causes of frequent ball valve failures. One example was to replace the carbon steel
accumulator tanks with stainless to eliminate rust as a potential ball valve failure
mechanism. In the meantime, the SERT established a monthly air drop test for each
of the airlock door sealing systems in lieu of the 18 month TS surveillance interval
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until confidence was established that the ball valves would not f ail, in addition, the
SERT implemented a weekly inspection for obvious leaks, which would precipitate
an immediate drop test.
c. _C_onclusions
After f ailures of the containment airlock door seal air ball valves, the licensee
appropriately formed a SERT to determine the root causes and recommend -
permanent corrective action. Actions already implemented as well as those
recommended appeared to be appropriate to correct the problem. Maintenance
technicians performed the work and postmaintenance testing in an excellent
manner.
M1.4 Missed Surveillance on Hvcroaen Mixina Valves
a. Insoection Scone (61726)
The inspectors evaluated the licensee's response to CR 96-2033,which identified
that the licensee had not met the surveillance requirement to verify that the
hydrogen mixing valves were closed every 31 days.
b. Observations and Findinas
On December 2,1996, during a procedure review to implement a TS change, the
licensee discovered that TS SR 3.6.5.3.2 was not implemented by Procedure
STP-000-0201," Monthly Operating Logs," Revision 15, as indicated by the
licensee's TS/ surveillance procedure cross-reference matrix. TS SR 3.6.5.3.2
requires the licensee to verify that the hydrogen mixing valves were in the closed
position every 31 days. The licensee reviewed other similar procedures and could
not identily any procedure in which the requirements of TS SR 3.6.5.3.2 were met.
Operators entered TS SR 3.0.3, which allows the licensee 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> to perform a
missed surveillance before declaring the LCO not met. Operators verified that all of
the hydrogen mixing valves were closed and the licensee exited TS SR 3.0.3.
The investigaJon revealed that during the development of the improved TS, an error
in renumbering the new surveillance requirements was made such that the
TS/ surveillance procedure cross-reference was in error. The licensee also noted that
prior to February 1996, the valve position of the hydrogen mixing valves was i
verified daily, to track the amount of time that the valves were open in accordance
with Procedure STF-000-0001," Daily Operating Logs." However, because the I
improved TS no longer required the licensee to track the amount of time that the
hydrogen mixing valves were open, the licensee deleted the daily valve position )
verification of the hydrogen mixing valves. 1
The licensee f ailed to satisfy the requirements of TS SR 3.6.5.3.2 from February to
December 1996. However, this f ailure to meet the TS was mitigated because
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operators verified the position of the hydrogen mixing valves during the quarterly
operability surveillance test of the hydrogen mixing fans. Therefore, the licensee
had reasonable assurance that the valves were closed during the time period that
the surveillance was missed.
For corrective action, the licensee corrected their TS/ surveillance procedure matrix
and performed a review of the improved TS to ensure that no other TS renumbering
errors occurred.
The f ailure to verify the hydrogen mixing valves closed every 31 days is a violation
of TS SR 3.6.5.3.2. This licensee-identified and corrected violation is being treated
as an NCV consistent with Section Vll.B.1 of the NRC Enforcement Policy. l
Specifically, the violation was identified by the licensee, was not willful, actions
taken as a result of a previous violation should not have corrected this problem, and
appropriate corrective actions were completed (50-458/9617-01).
c. Conclusions
An NCV was identified for f ailure to implement TS Surveillance Requirement 3.6.5.3.2, which required monthly verification that the hydrogen mixing valves
wre closed. The licensee made an error in renumbering requirements for the
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improved TS, which resulted in an incorrect procedure being referenced in the
'TS/ surveillance procedure cross-reference matrix.
M1.5 Missed Surveillance on Scram Accumulators
a. insoection Scoce (61726)
The inspectors evalua:ed the licensee's response to CR 96-2046, which identified
that the licensee had not met the surveillance requirement to perform a channel
functional test on the associated alarm circuit for each control rod scram
b. Observations and Findinas
On December 5,1996, during a procedure upgrade technical review, the reviewer
discovered that the testing methodology used for the channel calibration and
channel functional test of scram accumulator pressure and leakage alarms, '
respectively, did not test all circuits between the transmitters ar d the common
alarm located in the control room. Procedure STP-500-4201," Control Rod Scram j
Accumulator instrumentation 18 Month Channel Functional and 18 Month Channel j
Calibration," Revision 6, was revised in June 1994 to test the common alarm only ;
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once from one accumulator. The procedure reviewers assumed that sufficient
overlap was provided through the RC&lS system continuous diagnostic; however,
the procedure upgrade reviewer noted that not all of the alarm logic was being
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tested for each of the 145 accumulator transponder circuits. The AND gate for the
- pressure and leakage alarm was not tested by the self-diagnostic.
The operators entered Technical Requirements Manual SR 3.0.3, which allowed
declaring the accumulators inoperable to be dr,iayed for 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> to permit
accomplishment of the surveillance test. Prr,cedure STP-500-4201, Revision 7, was
changed and within the 24-hour period, all 145 accumulator circuits were
satisfactorily tested for common alarm annunciation. The inspectors observed
portions of the performance of the revised surveillance test and found no problems.
The procedure upgrade project is a corrective action commitment in progress for
previously identified inadequacies in surveillance test procedures. This process has
been effective in making improvements in technical content, usability, and format, i
Utilizing reviewers with technical experience and expertise in the instrument and i
controls area has enhanced this effectiveness as demonstrated by the appropriate
identification and dispositioning of this issue. For additional permanent corrective
action, maintenance management had discussions with the instrument and control
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technicians to reinforce sensitivity toward digital control and alarm systems. l
Failure to maintain Procedure STP-500-4201 technically adequale is a violation of-
TS 5.4.1.a. This licensee-identified and corrected violation is boing treated as an
NCV consistent with Section Vll.B.1 of the NRC Enforcement Policy. Specifically,
the violation was identified by the licensee, was not willful, actions taken as a result
of a previous violation should not have corrected this problem, and appropriate
corrective actions were completed (50-458/9617-02).
c. Conclusions
The procedure upgrade review 0r demoristrated excellent performance in identifying
and documenting on a CR a missed survCllance requirement associated with the
control rod scram accumulator instrumente. tion testing. An NCV was identified for
failure to maintain the technical adequacy of the surveillance test procedure
implementing the requirement to test the common control room alarm from all of the -
M1.6 IST of the Division 11 SSW System
a. Insoection Scope (61726)
On' January 17,1997, the inspectors observed performance of Procedure
~ STP-256-6304," Standby Service Water B Loop Quarterly Pump and Valve Testing,"
Revision 8.
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b. Observations and Findinas
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The test was performed with satisf actory restats and the operators followed the
procedure in a step-by-step manner. During previous performances of SSW IST, the
licensee did not take vibration data at the locations specified in Attachment 4 of
Procedure STP-256-6304,which was discussed as a violation in NRC Inspection
Report 50-458/96-15. The licensee corrected the procedural deficiencies for the
test performance of January 17.
However, the inspectors noted that a sign on the entrance to the SSW pump roums
stated that the SSW pumps were not protected by suction strainers and provided
instructions that all gaps in the floor must be covered during work to preclude
dropping items into the SSW basin. The inspectors questioned the operators as to l
wh'y they did not cover the holes in the floor during SSW pump testing per the
posted sign. The operators stated that they did not notice the sign upon entry.
The inspectors determined that this sign was posted on the entry as corrective
action for CR 91-0362, generated in 1991, which identified an item dropped into
the SSW pump basin during a previous performance of SSW IST. The inspectors
informed the shift superintendent, who wrote CR 97-0043 to address the
inspectors' concerns with the effectiveness of the' corrective actions for
CR 91-0362.
The licensee's investigation revealed that none of the operators that frequently
entered the SSW pump rooms had previously noticed the sign requiring holes to be
covered. The inspectors noted that although the corrective actions for CR 91-0362
appeared to be ineffective for alerting personnel to take proper precautions to
prevent dropping items into the SSW basin, no items were known to have fallen
into the basin; therefore, the licensee appeared to have reasonable assurance of
operability. However, the inspectors noted that the SSW system was the most
important system with respect to risk significance in the licensee's individual plant
examination, which emphasized the importance of taking conservative precautions ;
to protect this system. The failure to implement instructions as corrective action to
preclude dropping items into the SSW basin is a violation of 10 CFR Part 50,
Appendix B, Criterion V (50-458/9617-03).
l c. Conclusions !
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A violation was identified for the failure to take effective corrective actions to
preclude dropping items into the standby cooling tower basin. Because SSW was
the most important system in the licensee's individual plant examination, this
violation emphasized the importance of taking conservative precautions to ensure
operability. The IST cf the Division il SSW pumps was otherwise performed
properly and in accordance with the procedure.
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! M1.7 Surveillance Test of LPCI Pumn C Pumo Start Loaic (61726)
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- On January 13,1997, the inspector witnessed performance of Procedure l
j STP-204-1302,"LPCI Pump C Start Time Delay Channel Calibration and Channel l
Functional Test," Revision 9A. The inspectors noted that the craf tsmen
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j consistently used good self-checking and sound electrical safety practices. The
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' surveillance was performed in accordance with the procedure and the data was
satisfactory.
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i M8 . Miscellaneous Maintenance issues (92902,92700)
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M8.1 (Closed) Violation 50-458/9525-03: Surveillance testing of the average power
l range monitors was not performed at the frequency specified by the TS.
- Amendment 74 of the TS, issued on August 2,1994, reduced the frequency of a
j number of surveillance requirements from weekly / monthly to quarterly; however,
i the surveillance interval for the flow biased, thermal power trip remained at 7 days.
i Immediate corrective actions to perform the surveillance tests and revise the
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implementing procedures were reviewed by the inspectors at the time. The results
1 were satisf actory. The licensee reviewed all surveillance requirements associated
j with Amendment 74 and found no additional deficiencies. In response to this
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violation, the licensee referred to Licensee Event Report (LER) 50-458/95-009 for
j permanent corrective actions. The LER stated that implementation of TS
j Amendment 81, which was the improved TS, on October 1,1995, resulted in
- severalimprovements such as improved format providing for unique surveillance
i requirement numbering, revised surveillance test procedure data base to facilitate l
} cross referencing specific surveillance requirements, and licensing proce'dures for !
I processing license document changes were significantly revised to support
- implementation of the improved TS. ,
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The above referenced corrective actions were not fully effective, as demonstrated l
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by the missed surveillances discussed in Sections M1.4 and M1.5 of this inspection
t report and in NRC Inspection Report 50-458/96-26. NRC Inspection Report
- 50-458/96-26 cited a violation for a breakdown in the licensee's surveillance testing ;
i program, which included similar examples of missed surveillances. The extensive .
- corrective actions implemented and planned by the licensee in response to that j
i enforcement action supersedes this item and the effectiveness of those actions will i
- be evaluated during a future inspection. l
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l M8.2 (Closed) LER 50-458/95-002: Deficient IST surveillance of EDG air receiver check
j valves because of an inadequate procedure.
!
- - On March 21,1995, the EDG system engineer identified that the surveillance
j procedures for verifying the operability of the Division I and ll EDG air receiver tank
- inlet check valves were deficient. The test incorrectly included nonsafety-related
j check valves in the test boundary. This LER was discussed and left open in NRC
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Inspection Report 50-458/96-16. One corrective action for this problem was to
train system engineers and other selected personnel who reviewed and verified IST
surveil 5nce procedures. When the inspectors reviewed the training records, they
found that 4 engineers were not trained in this regard. The LER was left open
pending completion of this training. After being informed of this observation by the
inspectors, the licensee documented the discrepancy in CR 96-2069. On
December 13,1996 training was provided for the 4 engineers plus one extra. The
inspectors reviewed the training attendance sheet. All system engineers who
reviewed IST procedures were trained.
Failure to perform IST surveillance testing of the correct skid-mounted check valves
in the EDG starting air system was a violation of former TS 4.0.5. This i
licensee-identified and corrected violation is being treated as an NCV consistent
with Section Vll.B.1 of the NRC Enforcement Policy. Specifically, the violation was
identified by the licensee, was not willful, actions taken as a result of a previous i
violation should not have corrected this problem, and appropriate corrective actions !
were completed (50-458/9617-04). l
M8.3 (Closed) LER 50-458/96-003: Engineered safety feature actuations because of
electrical protection assembly brecker trip. This event was discussed in NRC i
inspection Report 50-450/96-002,Section 2.2. An unresolved item was identified ;
which questioned industry practice for retesting breakers after they had been racked
out and then back in. The unresolved item was closed with no enforcement action -l
as described in NRC Inspection Report 50-458/96-05, Section 9.2.
Ill. Enaineerina
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E2 Engineering Support of Facilities and Equipment (37551)
E2.1 Outdoor Temoerature Effects on Secondary Containment Neuative Pressure
a. Insoection Scope
The inspectors evaluated the licensee's response to CR 96-1916, which was
initiated as a result of a design engineering review of previous CR 90-0673, which
pertained to the effects of extremely low outside temperatures on the ambient
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pressures required in secondary containment.
b. Observations and Findinos
NRC Information Notice 88-76, alerted licensees that the design of secondary
containment pressure control and monitoring systems may not have taken into
account the temperature-induced difference in pressure gradients versus elevation
when the atmosphere outside secondary containment was significantly colder than
the ambient temperatures inside. During unusually cold weather, if secondary
containment differential pressure was monitored and controlled near the lower
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elevations of the building, the differential pressure could be within TS limits in the
lower areas of the building; however, in the higher elevations the differential
pressure would be less negative or perhaps positive. This is because of the
difference in density between the inside and outside atmospheres. Consequently, j
after the postulated design basis loss-of-coolant accident (LOCA), radiation
exposures could be higher than originally calculated because of the increased time
there would be a positive differential pressure in the upper elevations of secondary
containment.
On November 6,1996, while updating calculations for standby gas treatment
system drawdown analyses for the purpose of converting the calculations over to a
new GOTHIC program, the design engineers reviewed the previous licensee
disposition of NRC Information Notice 88-76. The design engineers found that the
disposition confirmed that during cold weather, a slightly longer positive pressure
would exist in secondary containment at the start of a design basis LOCA, but the
exclusion area boundary thyroid dose would be less than the 300 REM established
by 10 CFR Part 100. The disposition stated that the concern addressed by NRC
Information Notice 88-76 was applicable but inconsequential to River Bend Station
and no further action would be taken. The design engineers found that the
licensing basis was not revised to reflect the increased positive pressure period or 1
the increased post-LOCA doses. ]
The design engineers determined by calculation that post-LOCA and postfuel- l
handling accident doses would be within the limits of 10 CFR Part 100, and control
room doses would be within the limits of 10 CFR Part 50, Appendix A, General ;
Design Criterion 19, and Standard Review Plan Section 6.4, as long as the outside
temperature did not go below 10F. As an immediate corrective action, the
operators were instructed to place the standby gas treatment system and the fuel
building exhaust filtration unit in servk,e whenever the outside ambient reached ;
10 F or below. The inspectors nuted that this low temperature extreme would
rarely be reached in the geographical area of River Bend Station. The licensee
stated that the bounding temperature of 10'F assumed a O psi differential at ground
level, an inside temperature of 85 F, and a relative humidity of 80 percent inside
and 0 percent outside. The insnectors questioned when, since startup in 1985, the
temperature was below 10 F. The licensee responded by producing meteorological
tower printouts that indicated on December 23,1989, the temperature dropped to
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7 F for about 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />. This had a negligible effect on the positive pressure period
l such that postulated dose limits would not have been exceeded.
l Until the differential pressure monitoring and alarm equipment could be modified to
j indicate the most conservative differential pressure, the design engineers provided
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curves indicating acceptable values of differential pressure as measured with
existing equipment as a function of outside temperature. The engineers developed
curves for the reactor building annulus, auxiliary building, and fuel building. The
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curves were incorporated into Procedure STP-000-0001," Daily Operating Logs,"
Revision 20. A 10 CFR 50.59 safety evaluation was completed in support of the
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change. The inspectors reviewed the change and the safety evaluation and found
them to be technically adequate.
For long-term corrective actions, the licensee was considering moving the
differential pressure monitoring and alarm equipment detectors to a higher elevation
and/or changing the setpoints to a more conservative value so that there would be
no problems with temperature-induced differences in pressure gradients in
c. Conclusions
Design Engineering demonstrated a good questioning attitude in reviewing the
licensee's 1990 response to NRC Information Notice 88-76, relative to possible
secondary containment positive pressures caused by low outside temperature
extremes. Immediate action to provide the operators with outside temperature
dependent acceptance criteria for secondary containment pressure was appropriate
to the circumstances pending implementation of permanent corrective action.
E2.2 Review of Facility Conformance to Uodated Final Safety Analysis Reoort (UFSAR)
Descriptions
A recent discovery of a licensee operating their facility in a manner contrary to the
UFSAR description highlighted the need for a special focused review that compares
plant practices, procedures and/or parameters to the UFSAR description.
While performing the inspections discussed in this report, the inspectors reviewed
the applicable portions of the UFSAR that related to the areas inspected. The
following inconsistency was noted between the wording of the UFSAR and the
plant practices, procedures and/or parameters observed by the inspectors:
While reviewing the UFSAR as it pertained to containment personnel air locks,
discussed in Section M1.3 of this inspection report, the inspectors noted a minor
inconsistency between the design description of the airlock door interlocks in the
UFSAR and the actual design. Section 3.8.2.1.3.2 of the UFSAR stated that the
airlock design is such that a failure of two devices / systems (double failure) is
required to place the doors in a condition where both doors could nol be opened
simultaneously, thus satisfying the single-failure criteria. The word not was
incorrect, in that the installed doors could be opened simultaneously in the event of
a double interlock failure.
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The licensee promptly initiated action to revise the UFSAR to delete the word nqt.
The licensee's response to this minor inconsistency was appropriate. No additional
documentation is required in this report.
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E8 Miscellaneous Engineering issues (92903)
E8.1 (Closed) Violation 50-458/9525-01: Failure to meet General Design Criterion 55.
The inspectors identified that a line connected to the low pressure core spray
system did not contain a locked closed manual valve or was not determined to be
acceptable on some other defined basis. For corrective actions, the licensee: (1)
performed a review to determine if any other lines had a similar problem and noted
that the residual heat removal system had a similar configuration, (2) identified the
containment isolation boundary and sealed closed the applicable valves, (3) revised
the applicable system operating procedures, (4) revised the UFSAR, and (5) revised
be engineering instruction that determined locking requirements. The inspectors
reviewed the licensee's documentation of corrective actions and determined that
these items were satisf actory. In addition, the inspectors verified that the valves in
question were locked in the field.
IV. Plant Support
R1 Radiological Protection and Chemistry Controls
R 1.1 General Comments (71750)
Throughout this inspection period, the inspectors observed performance in
radiological protection. For the activities observed, the inspectors noted that
personnel properly donned dosimetry and followed radiological postings. The
inspectors verified that a sample of radiation, high radiation, and locked high
radiation areas were properly posted and controlled.
S1 Conduct of Security and Safeguards Activities
S 1.1 General Comments (71750)
Throughout this inspection period, the inspectors observed security officers as they
performed their duties. The security officers were alert at their posts, security
boundaries were maintained properly, and entry screening processes were
performed properly at the primary access point. Except for one minor discrepancy
that was immediately corrected, the inspectors noted during night tours that the
protected area was properly illuminated. 1
P3 Emergency Preparedness Procedures and Documentation
Licensee On-shift Dose Assessment Capabilities (Tl 2515/134) I
P3.1
a. Inspection Scope
Using Tl 2515/134, the inspectors reviewed information regarding:
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- - Dose assessment commitment in emergency plan
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- On-shift dose assessment emergency plan implementing procedure
- On-shift dose assessment training
, b. Observations and Findinas .l
- On December 16,1996, the inspectors conducted an in-office review of the
emergency plan and implementing procedures to obtain the information requested
j by the temporary instruction. The inspectors conducted a telephone interview with
'
the licensee on December 17,1996, to verify the results of the review. Based on j
, the documentation review and the licensee interview, the inspectors determined i
' + that the licensee had the capability to perform on-shift dose assessments using real-
- time effluent monitor and meteorological data and that the commitment was
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. described in the emergency plan and implementing procedures.
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i c. Conclusions
i The commitment to perform onshift dose assessments was appropriately described
{ in the emergency plan and implementing procedures. Further evaluation of the
, information obtained udmq the Tl will be conducted by NRC Headquarters
personnel.
- V. Manaaement Meetinos
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X1 Exit Meeting Summary
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The inspectors presented the inspection results to members of licensee management at the . 1
conclusion of the inspection on February 6,1997. The licensee acknowledged the findings
presented,
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The inspectors asked the licensee whether any materials examined during the inspection i
should be considered proprietary. No proprietary information was identified.
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ATTACHMENT
SUPPLEMENTAL INFORMATION
PARTIAL LIST OF PERSONS CONTACTED
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Licensee
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J. P. Dimmette, General Manager, Plant Operations
M. A. Dietrich, Director, Quality. Programs
D. T. Dormady, Manager, Plant Engineering
J. Holmes, Superintendent, Chemistry
H. B. Hutchens, Superintendent, Plant Security
T. R. Leonard, Director, Engineering ,
D. N. Lorfing, Supervisor, Licensing I
C. R. Maxson, Senior Lead Licensing Engineer
J. R. McGaha, Vice President-Operations
W. P. O'Malley, Manager, Operations
W. H. Odell, Superintendent, Radiation Control
R. L. Roberts, Acting Manager, Maintenance
INSPECTION PROCEDURES (IP) USED
IP 37551 Onsite Engineer:ng
IP 61726 Surveillance Observations
IP 62707 Maintenance Observation
IP 71707 Plant Operations
IP 71750 Plant Support Activities
IP 9.700
. Onsite Followup of Written Reports of Nonroutine Events at
Power Reactor Facilities
IP 925 01 Followup - Operations
IP 92902 Followup - Maintenance
IP 92903 Followup - Engineering
Tl 2515/134 Licensee On-Shift Dose Assessment Capabilities
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ITEMS OPENED AND CLOSED l
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~ Opened :
50-458/9617-03 VIO Failure to implement effective corrective action !
(Section M1.6) i
Closed i
50-458/9525-01 VIO Failure to meet General Design Criterion 55 l
(Section E8.1)- I
50-458/9525-03 VIO Missed surveillance on average power range ]
monitors (Section M8.1) .
50-458/95-002 LER Deficient IST procedure for EDG air receiver. i
check valves (Section M8.2) I
50-458/96-003 LER Engineered safety feature actuations due to ;
electrical protection assembly breaker trip 1
(Section M8.3) ,
1
Opened and Closed 1
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50-458/9617-01 NCV Failure to verify hydrogen mixing valves closed every 31 days
(Section M1.4) i
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50-458/9617-02 NCV Failure to maintain Surveillance Test Procedure STP-500-4201
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technically adequate (Section M1.5)
50-458/9617-04 NCV Failure to perform IST of the correct check valves in the EDG
starting air system (Section M8.2)
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LIST OF ACRONYMS USED
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CR Condition Report ;
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EOG Emergency Diesel Generator
EOP Emergency Operating Procedure
IP inspection Procedure
IST Inservice Testing
LCO Limiting Condition for Operation
LER Licensee Event Report
LOCA Loss-of-Coolant Accident 1
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LPCI Low Pressure Coolant injection
MAI Maintenance Action item
NCV Noncited Violation
PDR Public Document Room 1
psig Pounds per Square Inch Gage
RC&lS Rod Control and Information System
SERT Significant Event Review Team
SR Surveillance Requirement
SSW Standby Service Water
TI Temporary Instruction
TLCO Technical Limiting Condition for Operation
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TS Technical Specification