ML23033A333

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Integrated Inspection Report 05000277/2022004 and 05000278/2022004
ML23033A333
Person / Time
Site: Peach Bottom  Constellation icon.png
Issue date: 02/02/2023
From: Jon Greives
NRC/RGN-I/DORS
To: Rhoades D
Constellation Energy Generation, Constellation Nuclear
References
IR 2022004
Download: ML23033A333 (1)


See also: IR 05000277/2022004

Text

February 2, 2023

David P. Rhoades

Senior Vice President

Constellation Energy Generation, LLC

President and Chief Nuclear Officer (CNO)

Constellation Nuclear

4300 Winfield Road

Warrenville, IL 60555

SUBJECT: PEACH BOTTOM ATOMIC POWER STATION, UNITS 2 AND 3 -

INTEGRATED INSPECTION REPORT 05000277/2022004 AND

05000278/2022004

Dear David Rhoades:

On December 31, 2022, the U.S. Nuclear Regulatory Commission (NRC) completed an

inspection at Peach Bottom Atomic Power Station, Units 2 and 3. On January 20, 2023, the

NRC inspectors discussed the results of this inspection with Ron DiSabatino, Plant Manager,

and other members of your staff. The results of this inspection are documented in the enclosed

report.

One finding of very low safety significance (Green) is documented in this report. This finding

involved a violation of NRC requirements. We are treating this violation as a non-cited violation

(NCV) consistent with Section 2.3.2 of the Enforcement Policy.

If you contest the violation or the significance or severity of the violation documented in this

inspection report, you should provide a response within 30 days of the date of this inspection

report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN:

Document Control Desk, Washington, DC 20555-0001; with copies to the Regional

Administrator, Region I; the Director, Office of Enforcement; and the NRC Resident Inspector at

Peach Bottom Atomic Power Station, Units 2 and 3.

D. Rhoades 2

This letter, its enclosure, and your response (if any) will be made available for public inspection

and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document

Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public

Inspections, Exemptions, Requests for Withholding.

Sincerely,

Digitally signed by Jonathan E.

Jonathan E. Greives

Date: 2023.02.02 11:21:44

Greives -05'00'

Jonathan E. Greives, Chief

Projects Branch 4

Division of Operating Reactor Safety

Docket Nos. 05000277 and 05000278

License Nos. DPR-44 and DPR-56

Enclosure:

As stated

cc w/ encl: Distribution via LISTSERV

ML23033A333

x Non-Sensitive x Publicly Available

x SUNSI Review

Sensitive Non-Publicly Available

OFFICE Rl/DORS Rl/DORS

NAME SRutenkroger JGreives

DATE 2/2/23 2/1/23

U.S. NUCLEAR REGULATORY COMMISSION

Inspection Report

Docket Numbers: 05000277 and 05000278

License Numbers: DPR-44 and DPR-56

Report Numbers: 05000277/2022004 and 05000278/2022004

Enterprise Identifier: I-2022-004-0039

Licensee: Constellation Energy Generation, LLC

Facility: Peach Bottom Atomic Power Station, Units 2 and 3

Location: Delta, PA 17314

Inspection Dates: October 1, 2022 to December 31, 2022

Inspectors: S. Rutenkroger, Senior Resident Inspector

C. Dukehart, Resident Inspector

L. Casey, Senior Allegations Coordinator

N. Eckhoff, Health Physicist

B. Edwards, Health Physicist

C. Hobbs, Reactor Inspector

K. Mangan, Senior Reactor Inspector

N. Mentzer, Resident Inspector

A. Turilin, Reactor Inspector

A. Ziedonis, Senior Resident Inspector

Approved By: Jonathan E. Greives, Chief

Projects Branch 4

Division of Operating Reactor Safety

Enclosure

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees

performance by conducting an integrated inspection at Peach Bottom Atomic Power Station,

Units 2 and 3, in accordance with the Reactor Oversight Process. The Reactor Oversight

Process is the NRCs program for overseeing the safe operation of commercial nuclear power

reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

Failure to Implement an Effective Maintenance Strategy for Unit 2 and Unit 3 Residual Heat

Removal System Agastat Relays

Cornerstone Significance Cross-Cutting Report

Aspect Section

Mitigating Green None (NPP) 71152A

Systems NCV 05000277,05000278/2022004-01

Open/Closed

The inspectors identified a Green finding and associated non-cited violation (NCV) of

Technical Specification (TS) 5.4.1.a, "Procedures," and Regulatory Guide (RG) 1.33, for

Constellation's failure to establish an effective maintenance strategy for Agastat control relays

in the safety-related residual heat removal (RHR) system at both Peach Bottom Unit 2 and

Peach Bottom Unit 3. RG 1.33, Appendix A, November 1972,Section I, requires in part, that

preventive maintenance schedules should be developed to specify inspection of replacement

parts that have a specified lifetime. The vendor specified lifetime is 25,000 operations or 10

years from the date of manufacture, whichever occurs first, which was exceeded for a Unit 2

RHR control relay that failed in October 2017 and was over 37 years old.

Additional Tracking Items

None.

2

PLANT STATUS

Unit 2 began the inspection period in end-of-cycle coastdown. On October 16 and 17, 2022, the

unit was down powered and then shutdown for a planned refueling outage (RFO). After

completing the refueling, the unit was restarted on October 29, 2022, synchronized to the grid

on October 30, 2022, and returned to rated thermal power (RTP) on October 31, 2022. On

November 2, 2022, the unit was down powered to 55 percent for a control rod pattern

adjustment and returned to RTP the following day. The unit remained at or near RTP for the

remainder of the inspection period.

Unit 3 began the inspection period at RTP. On November 18, 2022, the unit was down powered

to 58 percent for a control rod sequence exchange, scram time testing, main turbine valve

exercising and testing, and waterbox cleaning. The unit was returned to RTP the following day

and remained at or near RTP for the remainder of the inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in

effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with

their attached revision histories are located on the public website at http://www.nrc.gov/reading-

rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared

complete when the IP requirements most appropriate to the inspection activity were met

consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection

Program - Operations Phase. The inspectors performed activities described in IMC 2515,

Appendix D, Plant Status, observed risk significant activities, and completed on-site portions of

IPs. The inspectors reviewed selected procedures and records, observed activities, and

interviewed personnel to assess licensee performance and compliance with Commission rules

and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

Impending Severe Weather Sample (IP Section 03.02) (1 Sample)

(1) Unit common, the inspectors evaluated the adequacy of the overall preparations to

protect risk-significant systems from impending severe weather during winter weather

advisory on December 15, 2022

External Flooding Sample (IP Section 03.03) (1 Sample)

(1) The inspectors evaluated that flood protection barriers, mitigation plans, procedures,

and equipment are consistent with the licensees design requirements and risk

analysis assumptions for coping with external flooding on November 17, 2022

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (3 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following

systems/trains:

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(1) Unit 3, standby liquid control on November 9, 2022

(2) Unit 2, 'A' and 'C' high-pressure service water (HPSW) on December 5, 2022

(3) Unit 3, spent fuel pool cooling system on December 21, 2022

Complete Walkdown Sample (IP Section 03.02) (1 Sample)

(1) Unit common, standby gas treatment system on November 23, 2022

71111.05 - Fire Protection

Fire Area Walkdown and Inspection Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated the implementation of the fire protection program by conducting a

walkdown and performing a review to verify program compliance, equipment functionality,

material condition, and operational readiness of the following fire areas:

(1) Unit 2, reactor building drywell area, elevation 135', PF-24 on October 25, 2022

(2) Unit common, cable spreading and computer rooms, PF-78H, on November 7, 2022

(3) Unit 3, reactor building general area, elevation 165, PF-13J, on December 27, 2022

(4) Unit 3, reactor building high-pressure coolant injection (HPCI) room, PF-62, on

December 28, 2022

71111.06 - Flood Protection Measures

Inspection Activities - Internal Flooding (IP Section 03.01) (2 Samples)

The inspectors evaluated internal flooding mitigation protections in the:

(1) Unit 2, reactor building HPCI room on November 21, 2022

(2) Unit common, 'E-2' emergency diesel generator (EDG) room on December 22, 2022

71111.07T - Heat Exchanger/Sink Performance

Heat Exchanger (Service Water Cooled) (IP Section 03.02) (2 Samples)

The inspectors evaluated heat exchanger performance on the following:

(1) RHR heat exchanger 3AE024 cooled by HPSW

(2) EDG heat exchangers (air, lube oil, and jacket water) cooled by emergency service

water (ESW)

Ultimate Heat Sink (IP Section 03.04) (1 Sample)

The inspectors evaluated the ultimate heat sink performance on the following:

(1) Unit 2 service water, ESW, and HPSW system operation. IP 71111.07T, Sections

02.02.d.4, d.5, d.6 and d.7 were evaluated

4

71111.08G - Inservice Inspection Activities (BWR)

BWR Inservice Inspection Activities Sample - Nondestructive Examination and Welding

Activities (IP Section 03.01) (1 Sample)

(1) The inspectors verified that the reactor coolant system boundary, reactor vessel

internals, risk-significant piping system boundaries, and containment boundary are

appropriately monitored for degradation and that repairs and replacements were

appropriately fabricated, examined, and accepted by reviewing the following activities

from October 18, 2022 to October 25, 2022:

03.01.a - Nondestructive Examination and Welding Activities

  • Record review of manual ultrasonic testing of the reactor water clean-up

system pipe to elbow weld, 12-4-5 (NDE Report P2R24-UT-016)

  • Record review of manual phased array ultrasonic testing of the core spray

safe end to N5B nozzle dissimilar metal weld 14-B-27 (GE Report 172976)

  • Direct observation of manual testing of the core spray N-5B nozzle pipe to

safe end weld 14-B-41 (NDE Report P2R24-UT-005)

  • Record review of manual ultrasonic testing of the control rod drive N-9 nozzle

to cap dissimilar metal weld 3-I-19R (NDE Report P2R24-UT-010)

  • Record review of encoded phased array ultrasonic testing of the 2-inch level

instrumentation nozzle N16A (GE Report 129135)

Reports P2-VT-016 and P2-VT-032)

  • Welding activities associated with the permanent installation of the 6-inch

torus drain modification and 2-inch instrument piping located, under work

order (WO) 05209091. This included record review of radiography testing of

16 shop welds (W2 through W10 and W13 through W18) and liquid penetrant

and magnetic particle testing of field weld W33

  • Record review of visual test results of torus internal wetted surfaces (WO 05042561)

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01)

(1 Sample)

(1) The inspectors observed and evaluated licensed operator performance in the control

room during the planned Unit 2 shutdown for refueling on October 16 and 17, 2022,

and the subsequent startup on October 29, 2022

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

(1) The inspectors observed and evaluated licensed operator requalification training in

the simulator on November 14, 2022

5

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (2 Samples)

The inspectors evaluated the accuracy and completeness of risk assessments for the

following planned and emergent work activities to ensure configuration changes and

appropriate work controls were addressed:

(1) Unit 2, HPSW unavailable for intake bay cleaning on October 20, 2022

(2) Unit 2, RFO activities, including '2B' 125 Vdc station battery and 'E-42'

4 kV bus testing and maintenance, on October 25, 2022

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 03.01) (3 Samples)

The inspectors evaluated the licensee's justifications and actions associated with the

following operability determinations and functionality assessments:

(1) Unit 2, refueling water storage tank manual drain valve was difficult to operate on

October 18, 2022

(2) Unit common, 'E-124' transformer circuit breaker 2-54-1505 failed to close after the

'E-12' bus was reenergized on October 23, 2022

(3) Unit 2, 'A' core spray loop minimum flow valve did not indicate full open on

November 17, 2022

71111.18 - Plant Modifications

Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02)

(2 Samples)

The inspectors evaluated the following temporary or permanent modifications:

(1) Unit 2, modification accepting damaged threads as-is without repair on main steam

isolation valve (MSIV) '86C' on November 10, 2022

(2) Unit 2, 'B' and 'D' HPSW pump pressure reduction modification on

December 15, 2022

71111.19 - Post-Maintenance Testing

Post-Maintenance Test Sample (IP Section 03.01) (5 Samples)

The inspectors evaluated the following post-maintenance testing activities to verify system

operability and/or functionality:

(1) Unit 2, reactor core isolation cooling (RCIC) low steam pressure flow rate testing

following maintenance on October 26, 2022

(2) Unit 2, reactor protection system (RPS) motor-generated set voltage regulator and

relay replacements on October 27, 2022

(3) Unit 2, exercising of control rods following maintenance during P2R24 RFO on

October 29, 2022

6

(4) Unit 2, 'B' RHR pump discharge check valve packing replacement on

December 13, 2022

(5) Unit 2, 'B' and 'D' HPSW pump modification acceptance testing following pressure

reduction modification on December 19, 2022

71111.20 - Refueling and Other Outage Activities

Refueling/Other Outage Sample (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated Unit 2 RFO P2R24 activities from October 16 to

October 30, 2022

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance testing activities to verify system operability

and/or functionality:

Surveillance Tests (other) (IP Section 03.01) (3 Samples)

(1) Unit 2, 'E-12' 4 kV bus loss of offsite power and loss of coolant accident functional

test on October 24, 2022

(2) Unit 2, alternate rod insertion and recirculation pump trip logic system functional test

including scram air header venting and recirculation adjustable speed drive circuit

breaker trips, on October 27, 2022

(3) Unit common, 'E-3' EDG fast start and full load test on November 15, 2022

Containment Isolation Valve Testing (IP Section 03.01) (1 Sample)

(1) Unit 2, 'A' loop MSIV local leak rate test on October 19, 2022

RADIATION SAFETY

71124.01 - Radiological Hazard Assessment and Exposure Controls

Radiological Hazard Assessment (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated how the licensee identifies the magnitude and extent of

radiation levels and the concentrations and quantities of radioactive materials and

how the licensee assesses radiological hazards

Instructions to Workers (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated how the licensee instructs workers on plant-related

radiological hazards and the radiation protection requirements intended to protect

workers from those hazards

Contamination and Radioactive Material Control (IP Section 03.03) (2 Samples)

The inspectors observed/evaluated the following licensee processes for monitoring and

controlling contamination and radioactive material:

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(1) Workers exiting the radiological controlled area during a RFO

(2) Workers exiting the Unit 2 drywell

Radiological Hazards Control and Work Coverage (IP Section 03.04) (4 Samples)

The inspectors evaluated the licensee's control of radiological hazards for the following

radiological work:

(1) Unit 2, feed water pipe machining inside drywell

(2) Torus dive for filter inspection and desludging

(3) Unit 2, 'B' reactor water cleanup pump replacement

(4) Unit 2, cavity drain down and decontamination

High Radiation Area and Very High Radiation Area Controls (IP Section 03.05) (3 Samples)

The inspectors evaluated licensee controls of the following High Radiation Areas and Very

High Radiation Areas:

(1) Unit 2 drywell

(2) Locked High Radiation Area key lock box and log book

(3) Unit 2 torus entrance hatch

Radiation Worker Performance and Radiation Protection Technician Proficiency (IP Section

03.06) (1 Sample)

(1) The inspectors evaluated radiation worker and radiation protection technician

performance as it pertains to radiation protection requirements

OTHER ACTIVITIES - BASELINE

71151 - Performance Indicator Verification

The inspectors verified Constellations performance indicator submittals listed below for the

period October 1, 2021, through September 30, 2022:

MS05: Safety System Functional Failures (SSFFs) Sample (IP Section 02.04) (2 Samples)

(1) Unit 2 SSFFs

(2) Unit 3 SSFFs

MS06: Emergency AC Power Systems (IP Section 02.05) (2 Samples)

(1) Unit 2 Emergency AC Power Systems

(2) Unit 3 Emergency AC Power Systems

OR01: Occupational Exposure Control Effectiveness Sample (IP Section 02.15) (1 Sample)

(1) November 5, 2021, through October 24, 2022

8

PR01: Radiological Effluent Technical Specifications/Offsite Dose Calculation Manual

Radiological Effluent Occurrences (RETS/ODCM) Radiological Effluent Occurrences Sample

(IP Section 02.16) (1 Sample)

(1) November 5, 2021, through October 24, 2022

71152A - Annual Follow-up Problem Identification and Resolution

Annual Follow-up of Selected Issues (Section 03.03) (2 Samples)

The inspectors reviewed the licensees implementation of its corrective action program

(CAP) related to the following issues:

(1) Unit 2 safety relief valve (SRV)-71K nitrogen supply hoses fretting

(2) Unit 2 and Unit 3 Agastat relays for the RHR system, issue report (IR) 4059704 from

October 5, 2017

71152S - Semiannual Trend Problem Identification and Resolution

Semiannual Trend Review (Section 03.02) (1 Sample)

(1) The inspectors reviewed the licensees CAP for potential adverse trends in the third

and fourth quarters of 2022 that might be indicative of a more significant safety issue

INSPECTION RESULTS

Failure to Implement an Effective Maintenance Strategy for Unit 2 and Unit 3 RHR System

Agastat Relays

Cornerstone Significance Cross-Cutting Report

Aspect Section

Mitigating Green None (NPP) 71152A

Systems NCV 05000277,05000278/2022004-01

Open/Closed

The inspectors identified a Green finding and associated NCV of TS 5.4.1.a, "Procedures,"

and RG 1.33, for Constellation's failure to establish an effective maintenance strategy for

Agastat control relays in the safety-related RHR system at both Peach Bottom Unit 2 and

Peach Bottom Unit 3. RG 1.33, Appendix A, November 1972,Section I, requires in part, that

preventive maintenance schedules should be developed to specify inspection of replacement

parts that have a specified lifetime. The vendor specified lifetime is 25,000 operations or 10

years from the date of manufacture, whichever occurs first, which was exceeded for a Unit 2

RHR control relay that failed in October 2017 and was over 37 years old.

Description: On October 5, 2017, TS surveillance procedure ST-O-010-301-2, "A RHR Loop

Pump, Valve, Flow, and Unit Cooler Functional and Inservice Test," for Unit 2 was aborted

due to failure of the 2A RHR pump minimum flow valve, MO-2-10-016A, to operate

automatically at two different steps in the surveillance procedure. Operator action was taken

to manually open MO-2-10-016A following start of the '2A' RHR pump in step 6.4.9 to prevent

damage to the pump from overheating. MO-2-10-016A is a normally closed motor operated

valve credited with an active safety function to open upon start of the '2A' RHR pump, to

protect the pump when operating in low flow or shutoff head conditions, due to a reactor

pressure that is higher than the shutoff head of the pump. MO-2-10-016A must be capable of

9

opening after a 10 second time delay, when the pump breaker is closed, and high differential

pressure exists across the pump. This design feature assures the RHR pump will not operate

at a flow rate less than the minimum flow required for adequate pump cooling. TS 3.3.5.1,

"Emergency Core Cooling System (ECCS) - Instrumentation," Condition E.2 was entered on

October 5, 2017, for inoperable control logic associated with the '2A' RHR pump differential

pressure indicating switch, which controls the opening and closing of MO-2-10-016A, with an

action statement to restore the channel operable status in 7 days.

The direct cause for the failure of the minimum flow valve to open automatically when

required was determined to be the failure of the time delay relay 2-10-K84A. The K84A time

delay relay is a normally de-energized 125 VDC Agastat control relay. At the time of failure,

the K84A relay was determined to be 37 years old, as indicated by a calibration sticker on the

relay. This failure was classified as a Maintenance Rule Function Failure for loss of

equipment needed to support the RHR Low Pressure Coolant Injection function of the RHR

system, monitored at the single train level. The relay was replaced, TS 3.3.5.1, "ECCS -

Instrumentation," Condition E.2 was exited, and the system was returned to service on

October 9, 2017.

An extent of condition investigation conducted in IR 4059704 in November 2017 determined

that there were 12 time-delay relays of the same model as the K84A relay installed in the

RHR system on Unit 2 and Unit 3. The investigation also concluded that the relays were all

classified as non-critical components, in which the Performance Centered Maintenance

(PCM) template recommended no periodic replacement or preventive maintenance for these

relays, and that this was a correct classification. In October 2022, the inspectors determined

that 38 Agastat control relays on Unit 2 had no preventive maintenance schedule, or

replacement frequency specified. The Unit 3 RHR system also had 38 Agastat control relays

with no preventive maintenance schedule, or replacement frequency specified. This

maintenance strategy was adopted on April 20, 2017, before the RHR system relay failed in

October 2017 and is currently the maintenance strategy that is still in place for normally de-

energized Agastat control relays in the RHR system at both Unit 2 and Unit 3.

Constellation procedure ER-AA-200, Preventive Maintenance Program, Revision 6,

Attachment 5 provides guidance for developing a maintenance strategy for non-critical

components. Item 3 lists bullets for determining a reasonable change out frequency based on

the expected service life of a component. Item 3.c states in part, to understand the

consequence of failure, beyond that based on component classification. Item 3.e states in

part, to consider actual operating history of a specific sub-component. Item 3.f states to

consider industry experience with the component. Item 11 states in part, that preventive

maintenance tasks as recommended by PCM templates, do not supersede preventive

maintenance tasks defined by a regulatory required program, such as TSs, and until a

regulatory requirement is changed, the regulatory requirement takes precedence.

The vendor specified a qualified life of these relays of 25,000 electrical operations or 10 years

from the date of manufacture, whichever occurs first.

The inspectors reviewed internal and external operating experience to determine if similar

failed relays examples existed. IR 4228359 documents a case where relay 2-2E-K004 failed

during TS Surveillance S12K-1G-TDR-A1C2 for the Peach Bottom Unit 2 automatic

depressurization system logic system on March 11, 2019. This failure led to an unplanned

entry in TS 3.3.5.1, function 4c until the relay could be replaced. This relay was a TR model

Agastat relay that was normally de-energized and in service for 39 years, similar to the 2-10-

10

K84A relay failure in the Unit 2 RHR system in October of 2017. In their evaluation,

Constellation determined that the cause of the failure was "due to age-related degradation ...

Engineering evaluation A0038908 defines an expected service life of 40 years." In addition,

the failure was "consistent with findings documented in EACE 1422221 [Peach Bottom

evaluation in November 2012] ... Age-sensitive parts include the time delay potentiometer,

solder joins, and on-board capacitors." Based on this failure, Constellation developed actions

to replace 3 similar relays but did not address the relays in the RHR system. These operating

experience examples were not fully considered in the development of a maintenance strategy

for Agastat control relays in the RHR systems at Peach Bottom.

The Constellation maintenance strategy, as shown in the PCM template, was documented as

not required. It did not have a maintenance schedule, nor have a clear development of a

basis using the criteria shown in ER-AA-200 for use of industry experience, failure history,

and vendor information. There was additional opportunity to re-evaluate the strategy following

the failure in 2017. However, no failure analysis was performed on failed time delay relay 2-

10-K84A in the RHR system in 2017, therefore, information was not available to support the

guidance in ER-AA-200, Attachment 5, Item 3.

Corrective Actions: Constellation issued IR 4531974, to review procedure ER-AA-200-1001,

Equipment Classification, to determine if enhancements could be made to this corporate

procedure to ensure the procedure is in compliance with the Peach Bottom licensing basis.

Constellation issued IR 4536189, to perform a review of relevant operating experience, to

determine if a change to the current RHR system relay maintenance strategy is needed, and

if there are concerns with the service life of other Agastat relays at Peach Bottom.

Corrective Action References: IRs 4059704, 4228359, 4301690, 4531974, 4536189

Performance Assessment:

Performance Deficiency: The inspectors determined that not establishing a preventive

maintenance schedule, or effective maintenance strategy for Unit 2 and Unit 3 RHR system

Agastat control relays in accordance with TS 5.4.1.a, and as implemented in station

procedure ER-AA-200, was a performance deficiency that was reasonably within

Constellation's ability to foresee and correct.

Screening: The inspectors determined the performance deficiency was more than minor

because if left uncorrected, it would have the potential to lead to a more significant safety

concern. Specifically, Agastat relay failures in the RHR system have the potential to render a

single ECCS instrumentation channel, or single train of the RHR system inoperable per TS,

between quarterly surveillance tests. This performance deficiency is similar to Example 13.a

in NRC IMC 0612, Appendix E, "Examples of Minor Issues," dated January 1, 2021.

Significance: The inspectors assessed the significance of the finding using IMC 0609,

Appendix A, The Significance Determination Process (SDP) for Findings At-Power. The

inspectors utilized IMC 0609, Appendix A, Exhibit 2, "Mitigating System Screening

Questions," and answered "No" to Question 1: "If the finding is a deficiency affecting the

design or qualification of a mitigating SSC, does the SSC maintain its operability, or PRA

functionality?". The inspectors answered "No" to Question 2: "Does the degraded condition

represent a loss of the PRA function of a single train TS system for greater than its TS

allowed outage time?". The inspectors answered Yes to Question 3: Does the degraded

condition represent a loss of PRA function of one train of a multi-train TS system for greater

than its TS allowed outage time?

11

Specifically, TSs related to the RHR system had a 7-day allowed outage time (AOT) in 2017,

when the failure of the Agastat relay for '2A' RHR pump occurred. The last time operability of

the 'A' train of the RHR system was confirmed, was during performance of ST-O-010-301-2,

92 days before the October 5, 2017, surveillance. Therefore, past operability during this 92-

day period was unknown and undetermined, which is greater than the TS AOT of 7 days.

Therefore, in accordance with IMC 0609, Appendix A, a detailed risk evaluation (DRE) was

performed.

The Senior Reactor Analyst (SRA) used the Systems Analysis Programs for Hands-On

Evaluation (SAPHIRE), Revision 8.2.6, Peach Bottom Standardized Plant Analysis Risk

Model, version 8.80 to perform the DRE. The basic event, RHR-MOV-CC-F016A, MINFLOW

Valve 10-16A Fails to Open, was set to TRUE. This was performed to invoke a limited

common cause failure potential for the evaluation of the performance deficiency. Other RHR

motor operated valve failure probabilities were increased by an order of magnitude to account

for increased failure probability though current surveillance tests were satisfactory. The SRA

did not include recovery for proper identification and repositioning of the valve(s) by

operators. This is considered a bounding analysis for Unit 2 and would represent the potential

risk to Unit 3, separately. No failures were identified on Unit 3.

A 92-day exposure time was used to bound the degraded condition and performance

deficiency. The increase in core damage frequency (CDF) for the conditional increased failure

to open was calculated to be 9E-8/year for the internal risk contribution. The dominant core

damage sequence consisted of a postulated loss of 4kV E12 bus, containment failure with

loss of all injection, failure to recover the power conversion system, and common failure of

the RHR min flow lines. IMC 0609, Appendix A, "SDP For Findings At-Power," does not

require a detailed evaluation of external risk contribution for internal event CDF increases

below a 1E-7/yr threshold. Additionally, the impact on large early release frequency would not

change this risk determination. This issue was determined to be of very low safety

significance (Green) for the calculated increase in CDF/yr due to the degraded condition.

Cross-Cutting Aspect: Not Present Performance. No cross-cutting aspect was assigned to

this finding because the inspectors determined the finding did not reflect present licensee

performance.

Enforcement:

Violation: TS 5.4.1.a requires in part, that written procedures shall be established,

implemented, and maintained covering the applicable procedures recommended in RG 1.33,

Appendix A, November 1972. RG 1.33, Appendix A, November 1972,Section I, requires in

part, that preventive maintenance schedules should be developed to specify inspection of

replacement parts that have a specified lifetime. The vendor specified lifetime is 25,000

operations or 10 years from the date of manufacture, whichever occurs first, which was

exceeded in October of 2017 for failed Unit 2 RHR control relay, that was over 37 years old.

Contrary to the above, since April 20, 2017, the date the current maintenance strategy was

established, Constellation failed to develop a preventive maintenance schedule, or an

effective maintenance strategy for Agastat control relays in the safety-related RHR system, in

Unit 2 and Unit 3, that have a specified life per TS 5.4.1.a. This led to an aborted TS

surveillance test and entry into a 7-day limiting condition for operation action statement, in

October 2017.

12

Enforcement Action: This violation is being treated as a non-cited violation, consistent with

Section 2.3.2 of the Enforcement Policy.

Observation: Maintenance Strategy for Unit 2 and Unit 3 RHR System Agastat 71152A

Relays

The inspectors performed a detailed review of IR 4059704 from October 5, 2017, in which TS

surveillance procedure ST-O-010-301-2, "A RHR Loop Pump, Valve, Flow, and Unit Cooler

Functional and Inservice Test," for Unit 2 was aborted, due to failure of the '2A' RHR pump

minimum flow valve, MO-2-10-016A, to operate automatically at two different steps in the

surveillance procedure. The direct cause for the failure of the minimum flow valve to open

automatically when required, was determined to be the failure of the Agastat time delay relay

2-10-K84A, that was over 37 years old at the time of failure in 2017. The inspectors

interviewed station operators, system engineers, and maintenance engineers concerning the

event in 2017, and the current Constellation maintenance strategy that is in effect for Agastat

control relays. In addition, a meeting was held with Constellation corporate personnel on

Monday, November 7, 2022, to discuss how plant components are classified, using

Constellation corporate procedure, ER-AA-200, "Preventive Maintenance Program," and

potential enhancements that could be made to this procedure. The inspectors reviewed the

PCM strategy for 42 Agastat control relays in the Unit 2 RHR system, and 42 Agastat control

relays for Unit 3 RHR system. The inspectors identified a Finding and Violation of regulatory

requirements related to the Agastat control relay preventive maintenance strategy for the

safety-related RHR system at Units 2 and 3. Details of the Finding and Violation are

described in Inspection Results Section, NCV 05000277,05000278/2022004-01.

Observation: Unit 2 SRV-71K Nitrogen Supply Hose Fretting 71152A

The inspectors reviewed Constellation staff's corrective actions that were performed following

the identification of a leak in the nitrogen supply hoses to the Unit 2 SRV-71K. On May 16,

2021, Constellation staff identified the nitrogen leak was a result of two stainless steel (SS)

braided hoses rubbing and fretting which was caused by system induced vibration and a

failed tubing support clamp. The issue was entered into the CAP (IR 04424199).

On May 18, 2021, Constellation staff replaced the braided hoses and modified the installation

orientation such that the hoses will remain separated even if not restrained by the tube

support clamp. Following repair and testing, Constellation staff declared SRV-71K operable

and it was returned to service. In addition, Constellation staff updated the hose installation

procedure (M-C-700-600, Revision 2), the relief valve replacement procedure (M-001-006,

Revision 16), and the tubing support specification (NE-00008, Revision 2) to incorporate

detailed installation instructions. Lastly, Constellation staff developed a subsequent design

change (EC 636137) to the braided hose configuration and implemented the change by

installing new hoses on October 23, 2022, during the Unit 2 RFO.

The inspectors reviewed the WO for the interim repair that initially replaced the hoses and

returned SRV-71K back to service. The inspectors reviewed the CAP Evaluation and

resulting corrective actions, including the design and procedure changes. Finally, the

inspectors performed a walkdown of SRV-71K and reviewed the WOs for the permanent

repair (WO 05217981) and extent of condition (WO 05212374). The inspectors determined

the Constellation staff actions had identified the deficiencies that caused the SRV-71K

nitrogen leak and corrective actions and extent of condition reviews were adequate.

13

Observation: Semi-annual Trend Review by Evaluating Potential Adverse 71152S

Trends in the Third and Fourth Quarters of 2022

The inspectors conducted a semi-annual trend review by evaluating sample issues that

occurred in the third and fourth quarters of 2022. During the evaluation, the inspectors

verified the issues identified were addressed within the scope of the CAP. The inspectors

reviewed health reports and related databases for trends and considered prior issues while

performing routine walkdowns and attending the plan of the day meetings. The inspectors did

not identify any substantive adverse performance trends or repetitive equipment failures

during this time that were not already identified by Constellation.

The inspectors reviewed potential trends in human performance issues, station

communication challenges, fire-related issues, and equipment degradation. Of these, the

inspectors noted significant plant impacts from river conditions during the summer period.

Unit 2 main condenser fouling caused by river conditions required an abnormal number of

downpowers. In addition, numerous safety-related and non-safety-related river-cooled heat

exchangers in both units required cleaning during the period, some multiple times. The

inspectors reviewed Constellations monitoring of heat exchanger performance and observed

the results of some manual cleanings. The inspectors observed abnormally high amounts of

biological debris (shell remains) and silt but did not observe evidence of live clams within the

systems. Constellation identified and issued trend issue reports for the heat exchanger

fouling and, separately, the Unit 2 main condenser performance. The inspectors determined

that the identification of an adverse trend for consideration of long-term corrective actions to

improve performance was appropriate.

Based on the overall results of the semi-annual trend review, the inspectors determined that

Constellation had identified adverse trends at Peach Bottom Atomic Power Station before

they could become more significant safety problems. The inspectors continue to monitor the

CAP and maintenance effectiveness during routine inspection activities.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On January 20, 2023, the inspectors presented the integrated inspection results to

Ron DiSabatino, Plant Manager, and other members of the licensee staff.

  • On November 10, 2022, the inspectors presented the Unit 2 and Unit 3 RHR system

Agastat relays inspection results to Sarah Ramos, Senior Manager of Strategic

Engineering, and other members of the licensee staff.

  • On October 28, 2022, the inspectors presented the exit meeting for IP 71124.01 and

IP 71151 inspection results to Ron DiSabatino, Plant Manager, and other members of

the licensee staff.

  • On October 25, 2022, the inspectors presented the Peach Bottom Unit 2 ISI inspection

results to Marcellus Ruff, Manager of Peach Bottom Programs Engineering, and other

members of the licensee staff.

  • On October 12, 2022, the inspectors presented the Triennial Heat Sink inspection results

to David A. Henry, Site Vice President, and other members of the licensee staff.

14

DOCUMENTS REVIEWED

Inspection Type Designation Description or Title Revision or

Procedure Date

71111.01 Operability SE-4 Flood - Bases Revision 34

Evaluations

Procedures LS-AA-4 Preparedness for Extreme External Events Revision 0

OP-AA-108-111- Severe Weather and Natural Disaster Guidelines Revision 24

1001

OP-PB-108-111- Preparation for Severe Weather Revision 19

1001

SE-4 Flood - Procedure Revision 43

SY-AA-101-146 Severe Weather Preparation and Response Revision 3

71111.04 Corrective Action Condition Reports

Documents IR 04087639

IR 04409221

IR 04475047

IR 04404162

IR 04443607

Miscellaneous M-363 P & I Diagram Fuel Pool Cooling & Clean-Up Revision 44

Procedures M-315 P & I Diagram Emergency Service Water and HPSW Syss Revision 94

M-397 Standby Gas Treatment Control Diagram Revision 61

SO 19.8.A-3 Fuel Pool Cooling System Routine Inspection Revision 13

SO 9A.8.A Standby Gas Treatment System Routine Running Inspection Revision 6

SO 9A.8.B Standby Gas Treatment System Routine Shutdown Revision 3

Inspection

ST-O-011-350-5 SBLC Explosive Valve Charge Continuity Check and Valve Revision 2

Position Verification

ST-O-032-350-2 HPSW Valve Alignment Verification Revision 4

71111.05 Miscellaneous ECR 632254 PF-0007 REV 4AY- Cable Spread Room Revision 0

Procedures PD-12 Typical Penetration Seal Detail Protective Topping for Foam Revision 0

Seals (SF-60)

PD-5 Typical Penetration Seal Detail External Pipe or Conduit Revision 1

Seal (SF-20)

15

Inspection Type Designation Description or Title Revision or

Procedure Date

PF-0007 Combustible Loading Analysis Revision 5C

PF-13J, Unit 3 Procedures Revision 3

RX Building: Unit 3 RX Building, General Area - Elevation 165-0

General Area -

Elevation 165-0,

Revision 3

PF-24 Unit 2 Reactor Building, Drywell Area - Elevation 135'-0" Revision 6

PF-62 Unit 3 RX Building; HPCI Room - Elevation 88-0 Revision 7

PF-78H Turbine Building Common, Cable Spreading and Computer Revision 9

Rooms - Elevation 150-0

Work Orders C0259205 DEHC PENE TBC-15-302-2-6015/6015A ECR 14-00421 Revision 0

71111.06 Corrective Action IR 04415793 E2 Roof/roll-up door area leaks during rainfall

Documents

Miscellaneous ECCS Flooding

Analysis

Procedures M-518 Plumbing, Drainage Reactor Building Unit No. 2 Plan at El Revision 12

091ft-06in

71111.07T Engineering PM-0589 RHR Heat Exchanger Performance Evaluation Revision 7

Evaluations

Miscellaneous Peach Bottom Atomic Power Station, Unit 2 and 3 Response Date

to NRC Generic Letter 89-13, "Service Water System 01/29/1990

Problems Affecting Safety-Related Equipment"

ER-PB-450-1006- Structures Monitoring Inspection Checklist - Pump Structure Performed

F-0 Rooms 800, 801, 802, 803, 804, 805-807 6/17/2022

Work Orders 04268137-14 Eddy Current Inspection Report - A RHR Heat Exchanger Performed

(3AE024) 04/20/2021

04869085 01 performed

10/23/20

04988982 01 performed

10/29/21

RT-0-033-600-2 Flow Test of ESW to ECCS Coolers and Diesel Generator Performed

Coolers 8/27/22

RT-X-010-661-3 RHR Heat Exchanger Performance Calculation Test Performed

12/01/2021

16

Inspection Type Designation Description or Title Revision or

Procedure Date

71111.08G Corrective Action 04530721

Documents

71111.13 Corrective Action IR 4530982

Documents

Procedures SO32.7.A-2 Placing Unit 2 HPSW Loops In-Service Using Unit 3 HPSW Revision 16

Pumps

71111.15 Corrective Action 4530585

Documents 4531583

IR 04537592

Procedures ST-O-014-301-2 Core Spray Loop 'A' Pump, Valve, Flow and Cooler Revision 45

Functional and Inservice Test

ST-O-054-751-2 E-12 4kV Undervoltage Relays and LOCA Loop Functional Revision 27

Test

Work Orders WO 05084304

71111.18 Corrective Action CRs

Documents IR 04531434

Miscellaneous EC637808 AO-2-01A-086C Bonnet Stud Hole Threads Damaged Revision 0

ASME B1.1-2003 Unified Inch Screw Threads Reaffirmed

2008

EC 627497,

EC 627499

EPRI TR- Bolted Joint Maintenance & Applications Guide December

104213s 1995

NMP Design NCR LIM MSIV BOLTHOLE AS-IS, The Final NCR

report certification Disposition is Use-As-Is MSIV Drawing

SR 534 Technical Justification for the Acceptance of the Damaged Revision 1

Bonnet Studs of 2MSS*AOV6A, 6B, 6C, 6D, 7A, 7B, 7C, &

7D

Work Orders 04269685

04892413

04892415

71111.19 Corrective Action IR 04532568,

Documents IR 04532960

17

Inspection Type Designation Description or Title Revision or

Procedure Date

Miscellaneous EC 627497

Procedures GP-11.E RPS SCRAM and ARI Reset Revision 26

GP-8.C Groups I, II, and II Inboard Half Isolation Revision 22

SO60F.6.A-2 Transferring Reactor Protection System Power Supplies Revision 19

ST-O-003-561-2 Control Rod Exercise - All Rod Revision 20

ST-O-010-306-2 B RHR Loop Pump, Valve, Flow and Unit Cooler Functional Revision 57

and Inservice Test

ST-O-013-210-2 RCIC Low Steam Pressure Flow Rate Test Using Auxiliary Revision 5

Steam

Work Orders 04892413

04892415

05285285

05312953

71111.20 Operability M-004-400 Revision 51

Evaluations

Procedures GP-2-2 Normal Plant Start-Up Revision 27

GP-3-2 Normal Plant Shutdown Revision 27

GP-6 Refueling Operation Revision 41

71111.22 Corrective Action IR 4532631

Documents

Miscellaneous TCC 22-0034 ST-I-03B-105-2 Revision 16A

Procedures ST-I-03B-105-2 ARI/RPT Logic System Functional Test with Scram Air Revision 16

Header Venting and Recirc Breaker Trips

ST-O-052-413-2 E-3 Diesel Generator Fast Start and Full Load Test Revision 26

ST-O-054-751-2 'E-12' 4kV Bus Undervoltage Relays and LOCA Loop Revision 27

Functional Test

ST/LLRT MSIV LLRT Test Revision 20

20.01A.02

Work Orders 5106406

WO 05106306

71152A Corrective Action 04424884

Documents 4059704 MO-2-10-16A Not Opening on RHR Pump Start 10/05/2017

4219191 E434 LC Failed to Energize During a 4kV Bus Fast Transfer 02/11/2019

18

Inspection Type Designation Description or Title Revision or

Procedure Date

4301690 Relay PCM Template Change 12/05/2019

4393997 Found Relay 3-10A-K70A out of tolerance high 01/05/2021

Corrective Action 4531974 NRC ID: Component Classification IAW ER-AA-200-1001 10/25/2022

Documents 4536189 Agastat Relay PM Strategy Challenged 11/10/2022

Resulting from

Inspection

Miscellaneous Catalog 5- TE Connectivity, "Agastat E7000 Series, Nuclear Qualified Revised 3-13

1773450-5 Time Delay Relays"

Constellation Relays - Control / Timing Revision 1

Maintenance

Template

Constellation Relays - Control / Timing Revision 2

Maintenance

Template

ICES 424948 Exelon Maintenance Rule - Failure Classification Form, 11/17/2017

Peach Bottom Unit 2

Procedures ER-AA-200 Preventive Maintenance Program Revision 6

ER-AA-200-1001 Equipment Classification Revision 6

PI-AA-125-1003 Corrective Action Program Evaluation Manual Rev. 7

ST-I-010-100-2 RHR Loop A Logic System Functional Test 05/01/2018

ST-I-010-100-2 RHR Loop A Logic System Functional Test 12/02/2015

ST-O-010-301-2 "A" RHR Loop Pump, Valve, Flow, and Unit Cooler 10/05/2017

Functional and Inservice Test

ST-O-010-301-2 "A" RHR Loop Pump, Valve, Flow and Unit Cooler 05/17/2022

Functional and Inservice Test

Work Orders WO 05153522 SV-2-16-071K (RV-2-16-071K): Replace Hoses 05/18/2021

71152S Corrective Action Issue Report s

Documents (IRs)

4511479

4515678

4516673

4516882

4516882

4516918

19

Inspection Type Designation Description or Title Revision or

Procedure Date

4516918

4517287

4517287

4517290

4517290

4517290

4517998

4518779

4518811

4519330

4519951

4520173

4520180

4520301

4520301

4520301

4520488

4520991

4521141

4521519

4522738

4522745

4524364

4524476

4524658

4525857

4526146

4526147

4526154

20