ML20199G750

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Insp Repts 50-324/97-13 & 50-325/97-13 on 971109-1227. Violations Noted.Major Areas Inspected:Operations, Engineering,Maint & Plant Support.Includes Results of Maint, Engineering & FP Insps
ML20199G750
Person / Time
Site: Brunswick  Duke Energy icon.png
Issue date: 01/23/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20199G672 List:
References
50-324-97-13, 50-325-97-13, NUDOCS 9802040338
Download: ML20199G750 (50)


See also: IR 05000324/1997013

Text

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U. S. NUCLFAR REGULATORY COMMISSION

REGION 11

Docket Nos: 50-325, 50 324

license Nos: DPR 71. DPR 62

Report No: 50-325/97-13. 50-324/97 13

Licensee: Carolina Power & Light (CP&L)

Facility: Brunswick Steam Electric Plant, Units 1 & 2

Location: 8470 River Road SE

Southport, NC 28461

Dates: November 9 - December 27, 1997

Inspectors: C. Patterson Senior Resident Inspector

E. Brown Resident inspector

G. Guthrie, inspector in Training

J. Coley Reactor inspector (M1.3. M8.6)

J. Lendhan. Reactor Inspector (E1.1. E1.4. E5.1. E8.3.

E8.4. E8.5)

C. Doutt. Senior Instrumentation and Controls

Engineer. Office of Nuclear Reactor Regulation

(E1.1. E1.2. El.3)

G. Wiseman. Reactor Inspection (F2.1. F2.2. F2.3,

F3.1. F5.1 F6.1. F7.1)

Approved by: M. Shymlock. Chief. Projects Branch 4

Division of Reactor Projects

9802040330 900123

PDR

G ADOCK 05000324

PDR

Enclosure 2

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EXECUTIVE SUMMARY

Brunswick Steam Electric Plant. Units 1 & 2

NRC Inspection Report 50 325/97 13. 50-324/97-13

This integrated inspection included aspects of licensee operations,

engineering, maintenance, and plant support. The report covers a 6-week

period of resident inspection; in addition. It includes the resu'ts of

maintenance, engineering, and fire protection ir,pections by regional and

headquarters inspectors.

Operations

e The inspector concluded that u.e cold weather program has been

satisfactorily implemented. Adequate contingency plans and operator

checks for proper operation of the systems were noted in the procedures.

Section 01.1).

  • The inspector concluded. from a safety system walkdown, that the

Containment Atmospheric Dilution system was being maintained as designed

(Section 02.1).

  • The clearance reviewed was prepared. authorized, and implemented in

accordance with procedure (Section 02.2),

e The inspector concluded that the Plant Nuclear Safety Committee meeting

provided an effective review of Unit I readiness for restart (Section

07.1).

e Inspe.; tor review determined that clearance records were not retained in

accorcance with Technical Specifications (TS). The failure to maintain

clearance records in accordance with TS was a violation (Section 07.2).

  • The control of a short duration mid-cycle o:tage was excellent (Section

07.3).

  • Licensee investigation determined that removal of the IB Reactor

feedwater Pump at too high a power level caused larger than expected

level transients. These transients combined with the improper

functioning of the level contacts in the Reactor Recirculation Run back

logic circuitry, resulted in the November 5-6. 199/ run backs (Section

08.3).

  • The inspector concluded that the licensee's control of the 2C and 20

electrical bus maintenance was weak because they did not recognize DG in

oberabilityconditionsduringtheimplementationoftt.eirclearance

( ection 08.4).

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Maintenance

e Movement of the spent fuel shi) ping cask was perforrxo in accordance

with methodology approved by t1e NRC in a letter dated December 2, 1997.

Adequate supervisory oversight was present during movement of the cask

(Section M1.1).

  • The inspector observed performance of calibration of two Reactor Core

Isolation Cooling (RCIC) pressure switches. The work activities were

completed without any identified questions or concerns (Section M1.2).

  • Maintenance activities observed relating to equipmert qualification of

electrical equipment were found to be conducted in a thorough and

effective manner (Section M1.3).

. A violation was identified for a preventive maintenance procedure not

indicating specific E0 requirements. This omission resulted in

deficient Nelson flame seals in motor control centers not being detected

during scheduled preventive maintenance activities (Section M1.3).

  • The licensee continues to struggle with proper dispositioning of

abnormal indications. The failure to maintain the Daily Surveillance

Report in accordance with procedure was a violation. Abnormal values

observed fer the Steam Jet Air Ejector radiation monitor and subsequent

test indicated potential fuel failure for Unit 1 (Section M3.1),

  • The licensee identified that the Unit 2 Core Spiay sparger differential

alarm setpoints were outside of the TS allowable range. The cauce was

attributed to voiding of the sparger nozzles similar to the phenomenon

identified previously on Unit 1. The alarm setpoints were adjusted and

the associated documentation was updated (Section M8.5).

-Engineerino >

+ An additional example of a violation was identified for an inadequate

procedure for the conduct of E0 maintenance (Section E1.4). Two

inspector followup items were identified to review revisions to

instrument setpoint procedures and to review terminal block leakage

current evaluations (Section El.1 and Section E1.4).

  • A weakness was identified regarding a procedure reference to a drawing

for accident temperature data which was not available for use and

wording inconsistencies in the procedure (Section E1.1).

  • The licensee was making progress in resolution of the technical issues

and closure of CRs and JCOs (Section E1.4). The licensee training and

qualification for E0 personnel meets NRC requirements (Section E5.1).

Instrument setpoint calculations were technica ly adequate and complied

with NRC requirements (Section E1.2).

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Plant Support

. The ins)ector determined that each of the locked high radiation area

doors w11ch were checked were locked. lhe ins)ector concluded that the

licensee is satisfactorily controlling locked ligh radiation areas in

the plant (Section Rl.1).

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The inspector determined that several poor radiological work practices

existed in a radioactive material storage area (Section Rl.2).

The inspector found the status and condition of the protected area fence

i to be satisfactory (Section S2.1).

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Corrective maintenance on degraded fire protection systems was

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accomplished in a timely manner. The maintenance and material condition

of the fire protection equipment and features were satisfactory

(Section F1.1).

. The inspector concluded that silicone foam penetration seal field

verificction documentation was maintained by the licensee. The

inst 311ation and repair procedures for penetration seals provided

adequate guidance to ensure that materials were installed per design

requirements. However, the designs were not supported by seal testing

documentation, vendor data and inspection criteria, installer

qualification and training records, and engineering evaluations that

satisfy the guidance of Generic Letter 86-10 for deviations from the

fire barrier configuration qualified by tests (Section F2.2).

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The inspector concluded that fire door surveillance procedures and

acceptance criteria for verification of fire door clearances were in

accordance with National Fire Protection Association (NFPA) guidance.

However, an updated Final Safety Analysis Report (UFSAR) discrepancy

associated documentation of fire door and frame evaluations was

identified (Section F2.3).

. General housekeeping was satisfactory. Fire retardant plast.ic sheating

and film materials were being used. Lubricants and oils were properly

stored in approved safety containers. Controls for combustible gas bulk

storage and cutting and welding operations were being enforced.

Controls were being properly maintained for limiting transient

combustibles in designated separation zones and other restricted plant

areas (Section F3.1).

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The fire brigade organization and qualification training .act the

requirements of the site Procedures. Fire brigade turnout gear and fire

fighting equipment were being properly maintained (Section F5.1).

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The coordination and oversight of the tacility's fire protection program

had been reassigned from the previous Loss Prevention Unit organization

to shift. Operations. The new organizat.onal structure met NRC

guidelines and the licensee's fire protection program requirements

(Section F6.1). .

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. The 1997 Nuclear Assessment Section assessment of the facility's fire

protection program was comprehensive and was effective in identifying

fire protection program performance deficiencies to management. Planned

corrective actions in response tc the audit issues were substantial and

included a fire p.'otection reorganization (Section F7.1).

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ReDort Details

~ Summary of Plant Status

Unit I returned to power o)eration on November 14. 1997, following a mid-cycle

outage that began on Novem)er 5. 1997, to remove leaking fuel assemblies. Two

leaking fsel assemblies were identified and removed during the mid cycle

outage. However, indications of a potential fuel leaker remained after the

unit returned to full power operation. At the end of the report period the

unit had been on-line 42 days.

Unit 2 operated continuously during this report period. At the end of the

report period the unit had been on-line continuously for 59 days.

Due to concerns about the control room dose, the licensee imposed an

administrative limit on lodine until a Technical Specification (TS) amendment

submitted was a) proved. The licensee made a orocedure change to

Administrative procedure 0Al-81. Water Chemistry Guidelines, setting the limit

at 0.1 microcurie per gram dose equivalent L 'ine 131 compared to the TS value

of 0.2 microcurie per gram. Also, the licet ;e has been providing weekly

water chemistry data to NRR and the Resident Inspector for review. None of

the data reviewed has exceeded the administrative limit.

Due to a reconstitution of the Environmental Qualification (EO) program and

items identified, there are 12 of 24 Justification for Continued Operation

(JCO) that remain open for both units. The following provides the status of

the EQ JCOs and associated Engineering Service Requests (ESRs):

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1) ESR 97-00087. E0-Type JC0 for Improperly Configured Conduit Seal.

2) ESR 97-00574 Greyboot Connectors.

3) ESR 97-00329 (old ESR 96-00625). E0 Type JC0 for EQ Fuses Without

a Qualification Data Package (00P).

4) ESR 97-00289. Post A cident Sampling System (PASS) Valve Limit

Switch Panel Wiring.

5) ESR 97-00238. JC0 for Standby Gas Treatment Motor Operated Valve

(MOV) Position Indicator Rheostat.

6) ESR-97-00534. GE c' Type Terminal Strips.

7) ESR 97-00513. In-b Drywell Electrical Penetrations.

8) ESR 97-00535. Target Rock Solenoids TB Spray.

9) ESR 97-00449, Degraded Junction Boxes.

19) ESR 97-00250. Conduit Union in EQ Boundary.

11) ESR 96-00425. Evaluation of E0 sealants.

12) ESR 97-00523. High Pressure Coolant Injection Auxiliary Oil Pump

Motor Unit 1.

0P10

13) ESR 97-00446. GE Radiation Detectors. closure date to be

determined (TBD).

14) ESR 96-00503. Associated Circuit E0. closure date TBD.

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15) ESR 97-00330 (ola ESR 96 00501). Motor Control Center (MCC) E0 was

closed by the licensee, but was reopened - closure date TBD.

16) ESR 96-00426. Evaluation Quality class and E0 classification of

PASS valves was scheduled for completion June 6, 1997. but closure

date is TBD.

17) ESR 97-00529. Failure of Unit 1 Drywell Motor, closure date TBD.

18) ESR 96 00587 PASS Valves, closure date TBD.

19) ESR 96 00627 ODP for Marathon 300 Terminal Blocks was scheduled

for completion December 31, 1937 but revised to August 1. 1997,

but closure date is now TBD.

20) ESR 97-00229. JC0 for GE Condition Report (CR) 151 B Terminal

Blocks was scheduled to be completed September 1, 1997, but

closure date is now TBD.

21) ESR 97-00256. Main Steam Insulation Valve Hiller Aci . tor JCO. was -

scheduled for completion September 2, 1997. but closure date is

now TBD.

22) ESR 97-00343. Qualification of Kulka Model 600 Terminal Blocks was

scheduled for completion September 1. 1997, but closure date is

now TBD.

23) ESR 97-00435. MCC Fittings, closure date TBD.

24) ESR 97-00602. Solenoid Valve Field Wiring, closure date TBD.

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In summary Unit I returned to power operation following completion of a mid-

cycle outage. Unit 2 o)erated continuously; however there were 12

outstanding JCOs in the E0 area for both units.

I. Ooerations

01 Conduct of Operaticns

01.1 Cold Weather Preparation

a. Insoection Scone (71714)

The inspector reviewed the licensee's cold weather program to determine

whether it had been effectively implemented.

b. Observations and Findinas

The inspector reviewed the licensee's cold weather 3rogram for adequacy

and implementation by reviewing their Cold Weather 3111 and Freeze

Protection Procedure. Operating Instruction 001-01.02: Fire Protection

Procedure 0FPP-024. Freeze Protection of Fire Suppression System; and

Preventive Maintenance Procedure OPM-HT001. Preventive Maintenance on

Plant Freeze Protection and Heat Tracing. The inspector determined that

the procedures were adequately implemented. Additionally, the

procedures were adequately employed on multiple cold weather days. as

observed by the inspector.

The inspector conducted a walkdown of plant syn. , which were exposed

to cold weather. Systems which were heat traced were observed for

adequacy. The inspector looked for systems that did not have cold

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weather. heat trace installed. The inspector determined that the

operation of the Makeup Water Tank system heat trace was not controlled

by any procedure. The licensee stated that this heat trace system was

being controlled b," operator knowledge only. The licensee initiated a

procedure change request to place this heat trace system into their cold

weather procedures. The inspector noted on the Unit 2 Condensate

Storage Tank. High Pressure Coolant Injection (HPCI)/ Reactor Core

Isolation ~ Cooling (RCIC) level switch vent line that a six inch portion

of the lagging was missing at the top of the vent line and that the tin

shielding was missing around the lagging at an elbow on the vent line.

The lagging was wetted and degraded at the elbow. The inspector

discussed these two items with the licensee. The licensee did not

warrant these deficiencies as requiring corrective action. The

inspector did not find other systems requiring heat trace that were not

heat traced based on present system conditions and projected use of the

systems observed.

c. Conclusions

The inspector concluded that the cold weather program has been

satisfactorily implemented. Adequate contingency plans and operator

checks for proper operation of the systems were noted in the procedures.

02 Operational Status of Facilities and Equipment

02.1 Containment Atmosoheric Dilution (CAD) System Walkdown

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a. Insoection Scope (71707)

On December 10. 1997, the inspector performed a walkdown of the CAD

system in the Nitrogen and Off-Gas Services Building.

b. Observations and Findinos

The CAD system is described in Updated Final Safety Analysis Report

(UFSAR) Section 6.2.5. Combustible Gas Control in Containment. The CAD

system provides long-term nitrogen makeup after a Loss of Coolant

Accident (LOCA). This function is accomplished by vaporizing liquid

nitrogen and feeding it into containment as required to maintain an

oxygen concentration at or below five percent. The system is designed

to Engineered Safety Feature (ESF) standards, all equipment for CAD

service is designed with suitable redundancy and interconnections such

that no single failure of an active component will render the system

inoperable. This equipment includes one liquid nitrogen storage vessel.

two electric vaporizers, two flow-regulating stations. flow and

temperature indicators. and appropriate redundant valves and

interconnecting piping.

The inspector traced the system piping in the Nitrogen and Off-Gas

Services Building. The configuration was compared to plant drawing

0 02560. Containment Atmospheric Control System. The configuration was

found to be like the plant drawing. The inspector observed an inch of

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frost on the outside of the piping insulation on both sides of valve

HV-11. This valve is a manual isolation between the nitrogen tank and

an 85 pound pressure regulating valve.

The inspector questioned why the frost was on the line. The licensee

stated that the 90 pound relief valve setpoint was near the controlling

pressure of the 85 pound regulator and some nitrogen was venting off.

The redundant pressure regulating valve was isolated and it's isolation

valve (HV-12) was closed. The inspector questioned by keeping HV-12

closed, if the system was single failure proof. The licensee initiated

CR 97-04128. CAD Tank Isolation Valve, to address this issue, The

licensee concluded that no automatic action was required to address a

LOCA. Manual alignment of the pressure regulator was acceptable since

this was a long term post-LOCA action.

c. Conclusions

The inspector concluded, from a safety system walkdown, that the CAD

system was being maintained as designed.

02.2 Clearance Verification

l a. Insoection Scoce (71707)

The inspector reviewed the tagout for the Unit 2 Residual Heat Removal

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(RHR) system to verify proper clearance preparation, authori7 n. and

implementation,

b. Observations and Findinas

On December 10. 1997, the inspector performed verification of the proper

alignment and tagging of clearance 2-97-1781 on the Unit 2 RHR System.

All accessible components were verified to-be in the proper position

with the appropriate tags in place. The inspector reviewed Nuclear

Generation Group Standard Procedure OPS-NGGC-1301. Equipment Clearance.

The clearance package was adequately prepared, authorized, aad

implemer.ted. The inspector subsequently verified proper clearance

removal for those accessible components.

c. Conclusions

The clearance reviewed was prepared, authorized, and implemented in

accordance with procedure,

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07 Quality Assurarm in Operations

07.1 Restart Plant Nuclear Safety Committee (PNSC)

a. Insoection Scone (71707)

On November 11 and 12. 1997, the inspector attended the Unit 1 PNSC

restart assessment following a mid-cycle outage to replace two leaking

fuel assemblies,

b. Observations and Findinos

On November 11, 1997. PNSC was convened to review Unit I readiness for

restart. The committee reviewed the fuel sipping results and core

reload. Other maintenance activities during the outage were also

reviewed.

The meeting was conducted in accordance with TS with attendance by all

primary members, with no alternates. The meeting provided a thorough

discussion of all agenda items. The PNSC Chairman concluded that the

discussion of recirculation pump runbacks that occurred on November 5.

1997, during removal of the reactor feed pumps during the planned

shutdown was not complete. This item was statused as a restart

constraint requiring another PNSC review prior to restart. Noteworthy

in the review was the risk assessment review conducted for a failed

Control Rod Drive (CRD) pump. During the mid-cycle outage one of the

two CRD pump motors failed. The Probabilistic Safety Analysis (PSA)

person attended the comnittee meeting and presented the results from

running the risk assessment model considering failure of both CRD Jumps.

This risk was determined acceptable based on other TS required higi

pressure injection sources such as HPCI and RCIC.

On November 12. 1997, the inspector attended a second meeting. In this

meeting discussion was held regarding the problem with run backs and it

was concluded that this was due to a design deficiency that was already

corrected and installed on Unit 2 and scheduled for Unit 1 at the time

of the next refueling outage,

c. Conclusions

The inspector concluded that the PNSC meeting provided an effective

-review of Unit I readiness for restart.

07.2 Retention of Clearance Records

a. Insoection Scope (71707)

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The inspector reviewed whether configuration management documents,

specifically ciearances, were retained in accordance with TS 6.10. This

specification requires that facility records be retained in accordance

with the American National Standards Institute (ANSI) N45.2.9-1974

Collection. Storage, and Maintenance of Quality Assurance Records.

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b. Observations and Findinas

During ins)ector review of clearance errors which resulted in damage to

the Unit 23 recirculation pump seals, the licensee was unable to locate

a clearance hung to facilitate repairs on the recirculation motor oil- -

cooler. Tha clearance. 2-97-1531. was hung _resulting in a configuration

change for the B recirculation pump, but no maintenance on the system

was performed. The clearance was removed from the field, thus restoring

the system, and " rolled back" to allow use at a later date.

Subsequently, a scheduler requested the clearance be deleted due to the

repair activities being complete and approved without need for the

clearance boundary. As a result of the deletion of the clearance, no

record of the change in plant configuration was retained.

The inspectoi : viewed TS 6.10. UFSAR Section 1.8. Regulatory Guide

1,88, and ANS1 N45.2.9-1974. fhe inspector questioned the correctness

of not retaining the clearance. Since a configuration change did occur

despite the recirculation motor cooler activities not needing the cooler

isolated. Nuclear Records Management Procedure ORMP-001. Indexing of

Plant Records. defined those records required to be retained to satisfy

the 0A requirements stated in ANSI N45.2.9-1974. Discussion with the

licensee revealed that the records required to be retained did not

include clearances. The inspector reviewed the Nuclear Generation Grou)

Standard Procedure OPS-NGGC-1301. Equipment Clearance, and the Brunswicc

Required Records List. Neither document required that clearances be

retained.

TS 6.10 requires facility records shall be maintained in accordance with

ANSI N45.2.9-1974. ANSI N45.2.9-1974, in Section 3.2.7. Retention of

Records. states that Appendix A to the standard defined the types of 0A

records and the recommended retention periods. The failure to maintain

data sheets or logs on equipment alignment consistent with ANSI N45.2.9-

1974 is a violation. This violation is identified as VIO 50-325

(324)/97-13-01. Failure to Retain TS Required-0A Record.

c. Conclusion

Inspector review determined that clearance records were not retained in

accordance with TS. The failure to maintain clearance records in

accordance with TS was a violation.

07.3 Mid-Cycle Outaae (71707)

a. Insoection Scope

The inspector reviewed the mid-cycle outage activities to remove the

leaking fuel assemblies.

b. Observations and Findinas

Unit 1 was returned to power operation on November 14. 1997. This

completed a mid-cycle outage in eight days. The unit was shutdown.

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leaking fuel assemblies identified, removed, fuel reloaded and returned

to power o)eration. This short duration outage was the quickest on

record. T11s was accomplished with plant personnel without any major

problems. This outage was planned and controlled similar to a regular

refueling outage.

c. Conclusions

The control of a short duration mid-cycle outage was excellent.

08 Miscellaneous Operations Issues (92700, 92901)

08.1 (Closed) Unresolved Item (URI) 50-325/96-15-01: Vessel Disassembly

Without Secondary Containment.

During a refueling outage, the reactor vessel head and steam

dryer /separatorr assemblies were removed from the reactor vessel without

secondary containment integrity (SCI) established. This issue was

reviewed by the NRC Office of Nuclear Reactor Regulation. It was

determined that the removal of the nead and assemblies without SCI

established were not activities prohibited by TS 3.6.5.1. The potential

! for load handling accidents was a safety cuestion that has been reviewed

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by the NRC. However, maintenance of SCI curing vessel disassably was a

logical extension of the defense-in-depth ap3 roach used in addressing

the heavy loads issue and encouraged by the 4RC. The licensee's action

in proceeding with vessel disassembly was not conservative. The

licensee implemented controls during the Unit 2 refueling outage to

maintain secondary containment operable during vessel disassembly. This

issue was thoroughly evaluated as part of the licensee's Safe Shutdown

Risk Management Assessment.

08.2 (Closed) Violation V10 50-325(324)/97-02-01: Locked Valve Out of

Position

The licensee's response to this violation was dated May 5, 1997, and was

accepted by the NRC in a letter dated May 23. 1997. The corrective

actions described in the response letter were verified as complete by

the inspector. This violation is closed.

08.3 (Closed) URI 50-325/97-12-03: Recirculation Pumo Run backs

On November 5. 1997, the licensee began a c0ntrolled shutdown for the

Unit 1 forced outage in order to replace leaning fuel bundles. During

the shutdown. Unit I received two recirculation pump run backs to the 45

percent limiter. During the second run back the five percent buffer

region was entered and exited in accordance with procedures.

) Subsequently. no other transients or run backs were ercountered while

removing the Reactor Feedwater Pumps (RFPs) from service. The licensee

preliminarily attributed the first run back to a malfunction of the 1B

discharge check valve causing diversion of the 1A RFP through the 1B

discharge valve to the main condenser. The final analysis was provided

in the root cause analysis for CR 97-3917. Unit 1 Plant Transients While

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Removing a Reactor Feed Pump from Service. The inspector reviewed the

analysis and noted that the root cause attributed the run backs to the

removal of the RFPs at too high of a power level and a design problem in

the a) plication of the Metal-On-Silicon Field Effect Transistor (MOSFET)

switcl. The MOSFET was used in the 45 percent recirculation pump run

back logic to indicate the below 182 inches reacter water level contact

which is one of two contacts required to initiate the run back.

Reactor water level perturbations are expected during the removal of the

RFPs from service: however the magnitude of these perturbations seen for

these events were outside of the operators expectations. The root cause

analysis stated that removal of the RFP at 65 percent power was

inappropriate in that 65 percent during this evolution has changed since

power uprate. Before power uprate. RFPs were removed from service 3er

10P-32, Condensate and Feedwater System Operating Procedure, at or )elow

65 percent. Under current conditions 65 percent is approximately

equivalent to 68 percent power pre-uprated power. The analysis

attributed the magnitude of the perturbations to removal at too high of

a power level. In addition, the licensee determined that when the first

RFP was taken out of service, the less than 20 percent RFP flow contact

for the 18 pump was made up and with the MOSFET improperly indicating

below 182 inches water level the run backs were received. The design of

the MOSFET causes the contact to not be able to properly position itself

u'aon loss of the constant voltage supply. Therefore interruptions in

tle voltage will cause the MOSFET contact to not function as designed.

The second Run back was also attributed to the MOSFET. The licensee

intends to replace the MOSFETs in the next Unit 1 outage, The inspector

noted that the MOSFETs had already been replaced in Unit 2.

The licensee is reviewing plant operation to determine the appropriate

power level for removal of the RFPs from service. Based on licensee

satisfactory comaletion of the investigation into the cause for the

multiple run bac(s on November 5-6, 1997 this item is closed.

08.4 (Closed) URI 50-325(324)/97-12-04: Diesel Doeration Low Voltace Auto

Start Defeated

The inspector reviewed the licensee's root cause investigation CR 97-

03683, 4KV Bus 2C/2D Clearances. The licensee's investigation

determined that the number 3 diesel generator (DG) undervoltage relay

had been disabled in the same manrer as the number 4 DG during similar

maintenance activities on different days.

The inspector verified that the licensee did not exceed TS action,

limiting condition for operation, or time requirements for both

electrical bus maintenance activities. The inspector found that, on

October 9. 1997, the plant was under a TS action statement requirement

per TS 3.8.2.1. to restore the inoperable bus to operable within 8

hours, or be in hot shutdown within the next 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />. The electrical

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bus was not restored, in this case, for 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> and 58 minutes. This

plant condition was not recognized as a problem until the root cause

investigation was performed. The root cause investigation was found to

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be adequate. The ins)ector concluded that the licensee *s control of the

2C and 2D electrical aus maintenance was weak because they did not

recognize that the DG would be inoperable during the implementation of

their clearance. This item is closed.

II. Maintenance

M1 Conduct of Maintenance

M1.1 Spent Fuel Cask Movement

a. Inspection Scooe (62707)

The inspector observed transfer of the spent fuel shipaing cask from the.

117 foot elevation to the transport v'hicle and from t1e transfer

vehicle to the 117 foot elevation of the Unit 1 Reactor Building. s

b. Observations and Findinas

On December 8. 1997, the inspector observed the removal of the spent

fuel shipping cask, with fuel in the cask from the 117 foot to the 20

foot elevation in the Unit 1 Reactor Building. On December 15, 1997,

the inspector observed shipping cask movement, without fuel in the cask,

from the 20 foot elevation to the 117 foot elevation in the Unit 1

Reactor Building. During both evolutions the cask was transferred with

the valve box covers removed while being moved by the non-single failure

proof yoke. Approval for use of a non-single failure proof yoke for

movement of the cask with the valve covers removed was granted to the-

l licensee by the NRC in a letter dated December 2, 1997. Upon reaching

the transfer vehicle on December 8. 1997. the cask was wiped down to

reduce contami.1ation levels. During both movements the inspector noted

that the area was adequately posted for the radiological conditions

I present and i ealth pnysics personnel were present. The inspector noted

that adequate maintenance supervisory oversight was present for both

cask movements.

Subsequent surveys of the cask after removal from the Reactor Building

revealed that the shipment exceeded required limits. This event was

captured in CR 97-4161. S)ent Fuel Cask (IF-300). The cask was returned

to the Reactor Building w1ere additional decontamination was conducted.

The licensee attributed the contamination levels seen to leaching of the

contamination due to changing temperatures and weather conditions.

c. Conclusions

Movement of the spent fuel shi) ping cask was performed in accordance

with methodology approved by t1e NRC in a letter dated December 2. 1997.

Adequate supervisory oversight was present during movement of the cask.

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10

M1.2 RCIC Turbine Exhaust Diaphraam High Pressure Instrument Calibration

a. Insoection Scoce (61726)

The inspector observed the performance of Maintenance Surveillance Test

2MST-RCIC230. RCIC Turbine Fxhaust Giaphragm High Pressure Instrument

Channel Calibration, for the pressure switches 2-E51-PSH-N012A and 2-

E51-PSH-N012C.

b. Observations and Findinas

On December 24. 1997, with Unit 2 at 100 percent power the inspector

observed the channel calibration for RCIC pressure switches 2 E51-PSH-

N012A and 2-E51-PSH-N012C. The inspector verified that duriug the

performance of this channel calibration that HPCI and Automatic

Depressurization System (ADS) were o)erable and that no othar work

activities were being conducted whic1 could cause an inadvertent

isolation. This test verified that, upon sensing of a high pressure

condition between the t'arbine exhaust dia)hragms, an isolation signal is

sent in accordance with TS 4.3.2.1 and Ta)les 3.3.2-2(4.b.6) and 4.3.2-

1(4.b.6)

The inspector reviewed the work request / job order (WR/J0) AKNU 19 and

the governing procedure 2MST-RCIC230. The procedure in use was verified

to be the correct revision and the test instrumentation in use was

within the allowable calibration duration. The inspector observed the

' procedure in use at all work locations and adequate communication was

maintained throughout the test. The work observed was completed

satisfactorily with no observed concerns.

c. Conclusions

The inspector observed performance of cal:uration of two RCIC pressure

switches. The work activities were completed without any identified

questions or concerns.

M1.3 General Comments

a. Insoection Scone (62700)

The inspector examined the following work activities involving EQ

electrical equipment to verify maintenance implementation of EQ

requirements.

WR/JO 97-ALVT-002 Verified Calibration of Unit 1 Loop B Residual

Heat Removal (RHR) Service Water Pressure Switches Tag No.

1-SW-PS-1176 B and 1-SW-PS-11760

WR/JO 97-AGDR-002 Verified Calibration of Unit 1. Loop A. RHR Flow

Transmitter (1-E11-FT-N015A). Converter (1-E11-FY-5119A). Square

Root Converter (1-E11-FY-K600A)

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11

.

WR/JO 97-AAAS-002 Unit 2. Loop B. RHR Breaker Test in compartment

DM 5 of GE IC 7700 Series MCC 2XB-2 Division Il

b. Observations and findinos

The above work was ,m cformed with the work packages present and in

active use. Technicians were skillful, experienced, and knowledgeable

of their assigned tasks. However, on December 10, 1997, while observing

Instrumentation and Control (I&C) maintenance personnel perform work

activities in accordance with WR/JO 97-AAAS-002, the inspector noted

that one of the multiple cable electrical penetrations in the top of MCC

2-2XB-2 did not have Nelson flame guard putty on the inside surface as

required by Maintenance Procedure OMMM 016. Environmental Qualification

Maintenance Program. Revision 4. to properly seal the penetration. The

inspector examined the putty installation on the top of the MCC cabinet

for each of the penetrations and found the putty seal severely damaged

on a second multiple cable penetration. In addition, cables were loose

in both of the multiple cable penetrations. The applicable

Environmental Otalification Data Package (ODP). ODP 67, requires missing

or disturbed Nelson putty seals to be repaired or replaced. However,

the PM procedure used to maintain and inspect the MCC's (PM Procedure

OPM-MCC002. Revision 7. PM of GE Motor Control Centers and Switchboards)

did not have inspection requirements or acceptance criteria to ensure

that putty seals were properiy sealing the cabinets. On September 17.

f 1997, a three-year PM conducted on MCC 2-2XB-2 would have identified

l this discrepancy had procedure OPM-MCC002 included the acceptance

criteria for the Nelson flame seal putty. A subsequent inspection

performed on December 11. 1997 by the licensee, of 22 MCCs found an

additional three MCC cabinet penetrations with damaged Nelson putty

seals. In addition. 15 3ercent of the cables inspected in cabinet

penetrations had putty w1ich appeared not to fully adhere to the cable

in some areas. Failure of the procedure to implement E0 requirements

for Nelson autty seals is identified as VIO 50-325(324)/97-13-02.

Inadequate 3rocedure for the Conduct of E0 Preventive Maintenance.

c. Conclusions

Maintenance activities observed related to E0 of electrical equiament

were found to be conducted in a thorough and effective manner, iowever,

a violation was identified for a PM procedure not indicating specific E0

requirements. This omission resulted in deficient Nelson flame seals in

MCCs not being dettcted during scheduled PM activities.

M3 Maintenance Procedures and Documentation

M3.1 Steam Jet Air Eiector Off-Gas Radiation Monitor increase

a. Inspection Scoce (61726)

The inspector reviewed selected sections of Operating Instruction 101-

03.1. Control Operator Daily Surveillance Report to ensure that

i

1

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e

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12

appropriate and prompt actions were taken to address abnormal TS

surveillance values,

b. Observations and Findinos

On December 2. 1997. Unit 1 was in mode 1 at 100 percent power. The

inspector reviewed the daily surveillance report as contained in

Attachment 1 to 101-03.1 for November 30 through December 1. 1997. The

inspector noted that the values for the Steam Jet Air Ejector (SJAE)

i

off-9as radiation monitors on aage 26 were between 1570 and 1780

millirem per hour (mR/hr) whici was greater than the T3/ Operating Limit

value of 1000 mR/hr. The SJAE off-gas radiation monitors provide for

the detection of fuel element failures. The radiation levels are

recorded in 101-03.1 to provide an indication whether SJAE off-gas

radiation levels are approaching the alarm setpoint, which serves to

ensure that dose rates for gaseous effluents do not exceed the limits

l

prescribed in TS 3.11.2.1. Dose Rate.

l The inspector reviewed the associated procedures, work tickets, and

discussed the abnormal values with the licensee. Step 4.2 c 'f 001-03.1

required the control operator to red circle all values wt are not

within required limits. The inspector noted no indication on the

attachment or in the operator logs that action had been taken or was

expected to be performed to address the out-of-range values. Subsequent

reviews of the daily log entries by the inspector indicated continual

abnormal values and no red circles. These failures were recorded in CR

97-4136. Daily Surveillance Report. The failure to red circle values

not within required limits is a violation. This violation is identified

as VIO 50-325/97 13-03. Failure to Note Abnormal TS Surveillance Values.

CR 97-4100. Questioned OG Data / Fuel Leak indicated that on December 3,

1997, a step increase of approximately 200 mR/hr was seen on the

radiation monitor Subsequent sample results have shown an increase in

the Sum of Six value ano changes in the fuel reliability index which are

signs of potential fuel failure. In addition, the inspector noted that

incorrect sensitivities were used during the November 25, 1997.

adjustment of the SJAE radiation monitor alarm setpoilts. This was

documented by the licensee in CR 97-4046. SJAE Rad Mci. sensitivities.

CR 97-4180 SJAE rad monitor setpoints, addressed coordination problems ',

between the Operations procedure used to request new radiation monitor

setpoints, the Environmental and Radiological Control (E&RC) proced ce

that calculates the new setpoint, and the Maintenance procedure that

installs the new setpoints. By the time the radiation monitor setpoints

were ready to be installed the new values needed to be recalculated.

The inspector determined as a result of the cited failure and the three

additional CRs mentioned previously, that control and monitor'.ng of the

alarm setpoint was poor. Previous instances of failing to properly

disposition abnormal values were recorded by the NRC in Inspection

Re) ort (IR) 50-325(324)/97-12, when inadequate corrective action was

tacen for abnormally high drywell temperature. Tne abnormal temperature

resulted in exceeding the calculated environmental limits for ten

snubbers in the drywell.

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13

c. Conclusions

The licensee continues to struggle with proper dispositioning of

abnormal indications. The failure to maintain the Daily Surveillance

Report in accordance with procedure was a violation. Abnormal values

observed for the Steam Jet Air Ejector radiation monitor and subsequent

test indicate potential fuel failure for Unit 1.

M8 Miscellaneous Maintenance Issues (92902)

M8.1 (Closed) Licensee Event Reoort (LER) 50-325(324)/96-017-00: Invalid

Loss of Coolant Accident Locic Actuation

The invalid LOCA. initiation signal occurred during installation of test

equipment to support surveillance testing. P16nt systems responded as

designed. The initiation signal resulted in the following actuation:

Automatic start of emergency DGs 1.2.3. and 4.

Automatic start of Unit 1 Core Spray (CS) pump 1A.

Automatic start of Unit 2 Nuclear Service Water (NSW) pump 2A.

Unit 1 Grou) 10 division 1 actuation.

Closure of Jnit 1 Reactor Building Closed Cooling Water heat

exchanger Service Water isolation valve.1-SW-V106.

0)ening of NSW header to vital header isolation valve. 1-SW-V117.

, Slutdown of 1A and 10 Unit 1 drywell coolers  ;

1

Corrective actions, described in the LER. were reviewed and verified by

the inspector. -These included: appropriate administrative action with

the involved technician; briefing of maintenance 1&C technicians on this

event; providing maintenance I&C personnel managements expectations ft

the restart of surveillance tests after problems have been encountered;

restricting the use of Simpson Model 260 Voltage Ohm Meters (V0Ms) for

circuit checks specified in maintenance surveillance tests: developing

training to enhance technician knowledge of the effects of test

equipment misalignment: and revising maintenance procedures to preclude

similar events.

This event did not violate TS. This LER is closed.

M8.2 (Closed) LER 50-325/97-009-00: Missed Increased Frecuency Inservice

Testino Recuirement

The American Society of Mechanical Engineers (ASME) Boiler and Pressure

Vessel Code.Section XI, 1980 Edition through Winter 1981. Addenda

Section IWV-3414(a), requires an increase in test frequency in the event

an increase in stroke time of 25 percent or more from the previous test

is observed. Contrary to this requirement, the test frequency was not

increased as required. The required testing was missed by about two

weeks. Upon discovery. the valve was tested and the stroke time was

within the previous value and the test met the ASME Section XI

requirements.

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14

The corrective actions to prevent recurrence of this event. described in

the LER. were reviewed and verified by the inspector. Administrative

controls have been revised to ensure completed test results are reviewed

-in a timely manner and changes in test frequency are promptly initiated.

This event did not violate TSs. This event had minimal safety

significance from a-valve operability viewpoint since the retest of the

valve showed it was operable, ASME Section XI provides an intermediate

condition that allows continued operation without need for immediate

corrective action. From an administrative view, trending valve stroke

times is an imaortant indication of valve performance. Corrective

action taken s1ould improve this situation. This LER is closed.

M8.3 FClosed) LER 50-325/97-001-00: Rod Block Monitor Surveillance

.

nadeauacy

'

A discovery that the surveillance procedure fer testing the rod block

monitor (RBM). did not contain the pro 3er s 4

Ncessary to ensure  ;

testing of the RBM instrument channel 3 int '

tion, This condition

has existed since November 1996 for Unit 1, ma December 1996 for

'

Unit 2. Upon discovery, the correct tests were performed on both units

which indicated that the equipment was in calibration and capable of

performing its safety function.

The error was attributed to an inadequate administrative review of  ;

reformatting changes made in September 1996. The surveillance procedure

changes were being upgraded in accordance with the generic procedure

writers guide. However, these changes did not insert the proper steps

to test the RBM inop instrument channel B.

' Corrective actions, described in the LER. were reviewed and verified by

-the inspector. The inspector determined that this event did not violate

TS since only the test for channel B was missed. The situation was

corrected within the allowable time specified by TS 3/4.3.4.

The-results of the RBM inop functional tests performed on toth units

upon discovery, indicated that the equipment was in calibration and

capable of performing its intended safety function. This LER is closed.

M8.4 (Closed) LER 50-325(324)/95-022-00: HPCI System Discharae Flow Element

Gasket Leak

During performance of a post maintenance test on the HPCI system. the

discharge flow element flanged gasket developed a 5 to 10 gallons per

minute (gpm) leak. Several other problems were also observed with

system operation.

Investigation revealed that undersized flange studs had been originally

installed on the flow element flange, allowing the Flexitallic gasket to

be installed off center. The off centered gasket degraded during the

post maintenance test. This condition existed on both units and

prompted declaring a potential failure of the HPCI system to ]erform its

intended safety function. With the HPCI system inoperable tie TS

U

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15

oermitted continued reactor operation provide 1 the ADS. CS system, and

RCIC were operable. This event was withir, Me TS requirement.

Corrective measures as described in the LER were reviewed and verified

by the inspector. This LER is closed.

M8.5 (Closed) Ins)ection Follow-un item (IFI) 50-325/97-05-02: Abnormal CS

Soarcer Brea t Detector Indication

(Closed) VIC 50-325/97-06-03: Inadeauate CS Surveillance Procedure

.(Closed) LER 50-325/97 02: Core Soray Header Differential Pressure

Instrumentation InoDerable

On March 9.1997, en auxiliary o)erator (AO) was verifying

instrumentation indications in tie Unit 1 Reactor Building. The A0

observed.that the reading displayed for 1-E21-PDS-N004A. Core Spray Line

Break Indicator, was not within TS 4.5.3.1.2.c.2 requirements. This

)ressure switch functioned to detect a break in the CS piping located

l 3etween the vessel and the shroud. The differential pressure (dP)

sensor measures the pressure across the core. Due to the addition of

'

L the drop from the steam separator, any break in the line would cause the

l -

indicated pressure drop to increase which would cause a more positive

indicated dP. The out of tolerance condition had existed since

November 1996 as stated in LER 50-325/97-02. During review of the

associated surveillance procedures, the inspector determined that actual

verification of the CS sparger alarm setpoint in relation to the

" normal" indicated instrument pressure was not being performed.

L

I

Themfore. the licensee could not evaluate whether the alarm setpoint

was within the " normal" TS range. This nonconformance resulted in VIO

50 325/97-05-02. Inadequate CS Surveillance Procedure.

The licensee performed reviews of data collected nonroutinely during

1995-1996 and in ESR 97-181 calculated a " normal" value for setpoint

verification in the related surveillance procedures. The licensee

subsecuently changed the alarm setpoints and updated the affected

procec ures. Additionally. the licensee performed a review of the TS and

determined that appropriate logging of required TS values was being

accomplished. During the refueling outage for Unit 2 from Se]tember to

October 1997 the licensee, with prior NRC approval, uprated t1e 100

percent _ rated thermal power 5 percent. The licensee included

verification of CS sparger dP " normal" values as part of the uprate

test program performed in accordance with S)ecial Procedure 2SP-97-204.

Unit 2 Power Jprate Data Collection. The cleck served to record the CS

sparger shutdown values.

The inspector reviewed ESR 97-634. ESP-97-204. CR 97-3870. LER 50-

325/97-02, and other related documentation. The inspector verified that

routine recording. upon entering mode 1. of the CS sparger dP was

incorporated into 0)erating Instruction 001-03.3. Auxiliary Operator

Daily Surveillance Report for both units. CR 97-3870. Core Spray Leak

Detection, documented the discovery on October 29, 1997 by an AD, that

4

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16

the 2-E21-PDS-N004A. CS A Loop Leak Detection, was outside of its

specified range. The instrument was declared inoperable and an LC0 was

entered. The licensee determined the new CS dP range in ESR 97-634

Core Spr 3y Loop Line Breuk Detectio , Allowable Range Change. The new

alarm setpoints were implemented and integrated into the affected

surveillances. 3rocedures, and design documents. Based on completion of

the review of t1e TS for other " normal" values not properly trended,

adjustment of the dP alarm setpoints*to bring the setpoints into

rvpliance with TS. and the institution of routine monitcring of the CS

.qarger " normal" values these items are closed.

M8.6 (Clos (d) VIO 50-325(324)/97-02-04: Failure to Imolement the

Renuirements of (a)(1) and (a)(2) of 10 CFR 50.65. The Maintenance Rule

This violation reported that all historical data since July 10. 1993.

had not been obtained to establish baseline system / structure / component

(SSC) performance, validate scoping, and set initial condition (a)(1)

and condition (a)(2) in the case of the reactor protection system (RPS),

Only corrective work. requests / job orders had been used for initial

determination of functional failures. Therefore, instrument out-of-

calibration data had not been reviewed for the period of July 10. 1993

through October 30. 1995. As an action related to Maintenance Rule

implementation. Procedure OMMM-004. PM. was revised on October 30. 1995,

to require that out-of-calibration data be evaluated for Maintenance

Rule functional failure applicability. However, this requirement only

collected subsequent instrument out-of-calibration data.

As corrective action for this violation, the licensee reviewed all

available instrument out-of-calibration data for the RPS and other

components / systems which support the Maintenance Rule functions.

Functional failures identified were evaluated against performance

criteria to determine whether (a)(1) status should be assigned.

Although six condition reports were issued to evaluate additional

functional failures, no system was required to be classified (a)(1)

based on this review. The inspector reviewed the licensee's corrective

actions and held discussions with a)plicable management and engineering

personnel concerning this issue. T1e inspector concluded that the

licensee had taken the necessary corrective action to correct the

deficient condition and had taken appropriate corrective action to

prevent its recurrence. This item is closed.

III. Enaineerina

El Conduct of Engineering

El.1 Review of Enaineerina Procedures

a. Insoection Scoce (37550)

The inspectors reviewed the licensee's procedures which control the

environmental qualification program.

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4

4

17

b. Observations and Findinas

The inspectors reviewed the procedures listed below which control

various activities related to the environmental qualification 3rogram to

determine if the procedures implement the requirements of 10 C:R 50.

Appendix B. and 10 CFR 50.49. The following procedures were reviewed:

EGR-NGGC 0005. Engineering Service Requests. Rev 6. dated

Septembe" 5. 1997

EGR-NGGC-0007. Maintenance of Design Documents, Rev. 2. dated

August 22, 1997

'

EGR-NGGC 0153. Engineering Instrument Setpoints. Rev. 3. dated

August 22. 1997

l EGR-NGGC-0156. Environmental Qualification of mlectrical Equipment

l Important to Safety. Rev. 4. dated October 8.1997

ENP-13.6 Equipment Data Base System. Control and Revision

Rev. 12. dated June 25. 1997

MCP-NGGC-401.. Material Acquisition (Procurement Receiving, and

Shipping). Rev. 3. dated August 26, 1997

The inspectors verified that the procedures provided adequate

instructions for establishing, maintaining and implementing the

requirements of'10 CFR 00.49 except for the issues discussed

below.

Section 9.6 of procedure EGR-NGGC-0156 provided the guidance for

maintaining E0 qualification data packages (ODPs). The procedure

specified that changes to ODPs are to be captured using the ESR

process. The procedure required that ODPs were to be periodically

updated as necessary to maintain auditability, to incorporate new

'

requirements, to meet plant specific requirements, ard to keep the

number of outstanding-changes at a reasonable level. However

5

procedure EGR-NGGC-0156 did not specify a clear time requirement

for updating the CDPs. The inspectors also determined that

procedure EGR-NGGC-0007 did not provide any requirements for

updating ODPs. The failure to s]ecify specific criteria in

procedures could result in the 0)Ps becoming unauditable which is

contrary to the requirements of 10 CFR 50.49. The failure to

maintain and u]date the ODPs was one of the causes of the

violation whic1 resulted in the civil penalty identified in NRC

Inspection Report (IR) 50-325(324)/96-14. The failure to

establish clear, definite requirements for updating ODPs was

identified as a violation example at the Shearon Harris Nuclear

Plant in NRC IR 50-400/97-12. Since all Brunswick 00Ps are being

revised and updated at the current time, a violation was not

identified for this issue during the current inspection. The

licensee's corrective actions for the Harris plant will resolve

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18

this problem since the Harris. Brunswick, n.d H. B. Robinson

plants use the same corporate EGR-NGGC ?,ocedures.

Procedure EGR NG D 0153 provides the methodology to establish

instrument setpoint margins sufficient to account for various

instrument uncertainties and environmental effects including

temperature, pressure, radiation, seismic, and insulation

resistance errors

Although procedure EGR-NGGC-0153 provided guidance on the

treatment of environmental effects, the inspectors noted that in

the discussion of temperature effects, the applicability of vendor 3

worst case performance specifications to plant specific conditions i

was not clear. The inspectors also noted that requirements for

seismic effects in procedure EGR-NGGC-0153 were not clear

regarding t6 match / confirmation of vendor profiles to plant

specific [ les or configuration,

in addition, the inspectors noted that procedure EGR-NGGC-0153

referenced Drawing 0-03056. Service Environment Chart Normal &

Accident Conditions. Units 1 & 2. for information on accident

temperature data to be used in instrument setpoint calculations.

The inspectors determined that-Drawing D-03056 was " frozen" on

December 12. 1996, and was not available for use. The reason for

removal of Drawing 0-03056 from use was documented in CR 96-04002

which identif9d the need to revise. and update Drawing D-03056-to

incorporate f icironmental data from the Reactor Building

Environmentai Renort (RBER), Revision 5. The inspectors noted in

review of calculations initiated since December 1996, the RBER

was referenced for temperature profiles in the re:ctor building.

The licensee indicated that a revision to EGR-NGGC-0153 will be

initiated to resolve inconsistency in wording regarding the

application of accident temperature / seismic effects to make it

clear that vendor test results would fully envelope site specific

profiles unless an evaluation has been aerformed to evaluate the-

differences. Additional guidance will 3e included to characterize

the requirements for engineering reviews of test-data to ensure

seismic and environmental profiles are bounding for site specific

conditions. The licensee indicated procedure EGR-NGGC-0153 will

also be revised to either remove D-03056 as the reference for

temperature data and replace it with the appropriate reference

(the RBER) . or to correct the drawing.

The inspectors also identified that procedure EGR-NGGC-0153 unde-

Section 9.5.1. Calibration Errors, was not clear regarding

instrument calibration surveillance requirements for as-left, as-

found or leave-alone zone tolerances. The licensee indicated

that procedure EGR-NGGC-0153. Section 9.5.1. would be revised to

clarify these requirements to indicate that calibration tolerances

are the defined limits, above and below a desired value, within

which an instrument loop signal may vary and not require

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adjustment. Licensee engineers stated that calibration tolerances

are understood to be "as-left" values.

The inspectors will review Procedure EGR-NGGC-0153 in a future

inspection to followup on these issues. An ins)ector followup

item (IFI). 50-325(324)/97-13 06. Revisions to )rocedure EGR-NGGC-

0153, was identified to the licensee pending further review by

liRC.

c. Conclusions

With the exception of the issues discussed above, the inspectors

concluded that the licensee's procedures for implementation of the

Environmental Qualification com) lied with the requirements of 10 CFR

50.49 and 10 CFR 50. Appendix 3. An IFI was identified to review

procedure EGR-NGGC-0153 to verify that the licensee incorporates the

above comments and clarifications. The reference to a " frozen" drawing

to obtain accident temperature data and the wording inconsistencies

discussed above were identificd to the licensee as a weakness.

El.2 Review of Instrument Setooiit Calculations

a. Insoection Stone (37550) ,

The inspectors reviewed randomly selected instrument setpoint

calculations to deternine the adequacy of the licensee's calculations.

b. Observations and Finninos

The inspectors reviewed the instrument setpoint calculations

listed below and verified that the calculations were completed in

accordance with NRC requirements. The inspectors verified that

the calculations incorporated industry standards. Updated Final

Safety Analysis Report commitments. Technical S)ecification

requirements, and recommendations contained in iRC Regulatory

Guides. Calculations reviewed were as follows:

-

-Calculation OE41-0036. Power Uprate HPCI Steamline Flow High

Uncertainty and Scaling Calculation.

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Calculation ORWCU-0010. U1/U2 RWCU Flow Accuracy

Calculation. Units 1 and 2 RWCU Differential Flow Leak

Detection / BESS I&C.

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Calculation 0821-0068. Power Uprate Main Steam Line Flow

High Setpoint Uncertainty and Scaling Calculation.

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Calculation 0-01534A-297. Insulation Resistance Degradation

Calculation.

From review of System Description SD-01.2. Reactor Vessel

Instrumentation. and the Safety Evaluation by the Office of

, _ _ _ _ _ _ _ _ _ a

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20

Nuclear Reactor Regulation. Conformance to Regulatory Guide 1.97

Revision 2. Brunswick Steam Electric Plant. Units 1 and 2. Dated

May 14. 1985. the inspectors concluded that these calculations

were. typical. The instrument setpoint calculations typically

considered 140 F as the maximum temperature in the calculations.

From review of the calculations, the inspectors determined that

instruments that perform a safety function are analyzed for a LOCA

environment in the reactor building. The calculations showed that

instrument uncertainties considered instrument temperature effects

for a maximum temperature of 140' F which is bounding for the

analyzed LOCA environment.

The inspectors also determined that instruments relied upon to

mitigate the effects of a high energy line break (HELB) were also

evaluated by the licensee. For this instrumentation,

environmental uncertainties-for a harsh environment were not

required to be considered since the instrumentation function would

occur before the reactor building temperature )rofiles listed in

p the Reactor Building Environmental Report (REBR) Revision 6.

dated November 5. 1997, would reach 140 F and affect instrument

performance. The ins)ectors noted that abnormal temperatures were

not discussed in the-RBER. Discussions with licensee engineers

disclosed that the design base accident event is based on an

initial building environment airspace temperature of 104 F. The

building temperatures ace measured and recorded daily by plant

operators in accordance with procedure numbers 101-03.4.1 and 201-

03.4,4. Unit 1 and 2 Control Operator Daily Check Sheets.. The

= operators are required to contact the duty engineer when the

reactor building temperature exceeds 104 F so that engineering

can perform an assessment of the effects of temperature on

environmental qualification.

-The inspectors noted that calculations for instrumentation which

mitigates a HELB demonstrated that the instrument and associated

equipment would not be exposed to a harsh environment before the

instrumentation performed its safety function. In the instrument

calculations reviewed by the inspectors instrument setpoints were

based on a maximum temperature of 140 F (non-steam environment).

Although allowances were not made for a harsh environment. a

seismic allowance was included in the calculations.

Review of the temperature profiles as shown in the Brunswick

Reactor Building Environmental Report showed that the actuation

isolation signal would occur before exceeding the temperature

allowances assumed in the setpoint uncertainty calculations. An

exce) tion was the High Pressure Coolant Injection (HPCI) line

breat in the steam tunnel where the temperature profile showed

that 140 F would be exceeded for ap3roximately 2.5 seconds before

the isolation trip _ signal occurs. iowever this instrumentation

would remain operable based on thermal delays. However, the HPCI

isolation function would most likely be initiated by temperature

.

21

sensors in the steam tunnel or HPCI room which would occur

imediately with no time delay.

The inspectors concluded that the instrument setpoint calculations

complied with NRC requirements and were technically adequate.

Review of the calculations showed that environmental effects,

j- specifically accident temperature, were correctly evaluated in the

calculations,

c. Conclusions

The inspectors concluded that the licensee's calculations were

technically adequate and complied with NRC requirements. The

inspectors concurred with the licensee's conclusions that the

setpoints for instruments relied upon to mitigate the effects of a

KLB did not require inclusion of uncertainties for a harsh

environment since the instruments perform their ft..iction before

being effected by the harsh environment. Setpoints for

instruments required for LOCA effects include the appropriate

environmental uncertainties.

-El.3 Enaineerina Service Reaucst (ESR) 97-00426

a. Inspection Scoce (375501 '

The inspectors reviewed ESR 97-00426 which was prepared to address

questions on instrument setpoints.

b. Observations and Findinas

A review of procedures and various documents by an independent

consultant resulted in questions involving environmental effects

including uncertainties on instrument accuracy. These guestions .

were dccumented in an E-mail message dated June 20, 1997 Subject: '

E0 and Instrument Accuracy. The licensee addressed the referenced  !

memo in Engineering Service Request ESR 97-00426. Revision 0.

-dated September 18. 1997. ESR 97-00426 documents the evaluation

completed by the licensee to address environmental effects on-

instrumentation. The inspectors noted that the licensee response

did not address the questions in the June 20, 1997 E-mail message

point by point. but provided an evaluation that was more generic

in nature. The inspectors noted that ESR 97-00426 was an

engineering disposition (ED) type ESR. as defined in procedure

EGR-NGGC-0005. The use of this type ESR to respond to the E-mail

cuestions was appropriate since the ESR only communicated existing

cesign requirements, did not produce design output, and did not

change existing engineering documents.

The ESR concluded that instruments that aerform a safety function

are analyzed for a LOCA environment in t1e reactor building. The

instrument uncertainties consider -instrument temperature ef fects

for a maximum temperature of 140"F which is the maximum bounding

. . . .

..

. . . . .

.

.

.. - .

o

_ _ _ - _ - . _ _ _ _ _ _ _ . .

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_ ..

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22

temperature for the analyzed LOCA environment. The inspectors

noted that the word minimum had been incorrectly used in the

fourth line, third paragraph in Section 2.0 of the ESR. The

licensee stated that they will correct this error when the ESR is

revised. as discussed below.

ESR 97-00426 also concluded that harsh environmental effects have

been appropriately accounted for in safety related uncertainty

calculations. The ESR concluded that the isolaticr. aquence for a

HELB due to main steam line break. reactor core isolation cooling

l steam-line break, high pressure coolant injection steam line

break, cr a piping failure in the reactor water cleanup system is

such thtt the isolation function will occur before the

instrumentation is exposed to harsh environmental effects. This

conclusion was based on the instrumentation being able to perform

its safety function prior to the temperature exceeding the

temperature allowance assumed in the setpoint calculations. For

area temperatures exceeding the setpoint temperature uncertainty

allowance, the use of emergency operating procedures (EOPs),

operator action, and local temperature instrumentation would

mitigate the event and provide the actions to determine and/or

maintain. reactor level during a LOCA or HELB.

When temperatures exceed the temperatures (140 F) assumed in the

setpoint calculations, plant operation is controlled through the

' COPS. A review'of E0P-03-SCCP Revision 5. Secondary Containment

Control Procedure, and 2EOP-LPC Revision 1. Level / Power Control,

shows that high area temperatures are an entry condition into

secondary containment control procedure E0P when area temperatures

exceed the maximum safe operating value requiring manual reactor

sCrdm.

E0P-03-SCCP Revision 5. refers the operators to Caution 1 to

determine reactor level instrumentation operability. A review of

Caution 1 disclosed that vessel level wide range instrumentation  ;

8B21 - LI - R604A/604B and C32 - PR - R609 are not to be used when

secondary containment temperature exceeds 140 F. This exclusion

was because the reference leg and associated instrumentation for

these loops are in secondary containment. E0P Caution 1 then

)rovided compensation data for the remaining level instrumentation

]ased on drywell tem]erature, reactor saturation limit, and

reactor pressure. iowever, for secondary containment

temperatures above 140 F. Caution 1 instrumentation may not be

o)erable with instrumentation exposed to temperatures greater

tlan 140*F during an event. In cases when vessel level can not

adequately be determined, the E0Ps direct the operators to

depressurize by initiating ADS and flood the vessel using low

pressure emergency core cooling systems.

.

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.. . .

.. .

. .

.

. .

. . . ,

- _ _ _ _ _ _ _ _ _ _ _ _ - _ _.

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23

c. Conclusions

The inspectors concluded that the licensee adequately addressed

the questions in the June 20. 1997 E-mail message regarding

instrument and E0 accuracy. However, the licensee stated that

_

they will revise F.SR 97 00426 to address each question and

recommendation ir. the E-mail message point by point to further

clarify their response to the concerns / issues raised in the

June 20, 1997 E mail message.

El.4 Environmental Qualificat%1

,

a. Insnection Scooe (37550.92903)

The inspectors reviewed the licensee's corrective actions for the

Environmental Qualification (FO) program, in response to findings

l identified during Self-Assessment numbers 95-0041 and 96-0271 and

the violations identified in NRC IR 50-325(324)/96-14.

b. Observations and Findinas

1) Review of E0 Equipment Data Base

The licensee's corrective actions to resolve the discrepancies in

the E0 program identified by NRC (See IR 50-325 324/96-14)

include corrections to and updating of the Equipment Data Base

System (EDBS). Numerous errors in EDBS had been identified and

corrected by the licensee since the inspection findings were

identified in IR 50-325(324)/96-14. The errors in EDBS were .

identified during E0 equipment walkdowns and review of various  !

data bases. In addition, numerous errors were identified in the

EQ zones listed in EDBS for the location where various components

were installed. These primarily occurred at. zone boundaries and

were being resolved during review of walkdown data.

The requirements for. recording and correcting E0 data in EDBS was

s)ecified in- CP&L procedures EGR-NGGC-0156 and ENP-33,6. The

-c1anges to EDBS to correct errors were processed using Form 100 of

ENP-33.6. The Form 100 was design verified in the E0 unit and was

then forwarded to appropriate personnel for entry into EDBS. All

EDBS data entries made were independently verified by personnel in

the Configuration Management group in the Design Control Unit.

The independent verification was performed to minimize o-

eliminate data entry errors. Additional corrections to EDBS were

ongoing to incorporate E0 walkdown ins)ection results and the

revisions to EQ qualification data paccages.

The inspectors reviewed some randomly selected revisions to EDBS

identified as a result of the E0 corrective actions and verified

the EDBS data had been corrected. The inspectors also discussed

the program for control of changes to EDBS with various licensee

personnel who perform the day to day system revisions. These

.

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_ _________ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

24

discussions disclosed that these individuals were cognizant of the

requirements for controlling and making corrections to EDBS.

2) Review of Qualification Data Packages

The inspectors reviewed a draft cop.f of Revision 4 of ODP No. 49.

titled. " Qualification Data Package For NAMCO EA180 Series Limit

Switches" to determine if it adequately demonstrated environmental

qualification for the safety related NAMCO switches for use inside

the drywell in accordance with 10 CFR 50.49 and appropriate

licensee E0 Prccedures. The package addressed the following:

qualification level (0588 Cat. I); tag numbers of equipment

covered in the QDP: test report aaplicability; similarity of test

specimens to installed equipment: E0 parameters. temperature,

pressure, relative humidity, radiation, chemical spray,

submergence; cualified life: E0 maintenance requirements; test

anomalies; anc operating experience items.

During review 3f the Draft ODP. the inspectors identified the following

questions / comments:

.

The text in the CDP indicates that there were five anomalies in

.

'

Qualification Test Report (OTR) 130 but only four anomalies were

discussed in the ODP.

l .

Attachment 2 to the ODP included a calculation for qualified life

l of the limit switches which was not signed as reviewed.

  • Differences were noted in the system component evaluation

worksheets (SCEW) for the same limit switches in the different

units.

  • Data was missing from some of the SCEW sheets. That is, there

were blanks on the data sheets. For example, data on accuracy was

left blank.

Some components were specified with Anaconda flex and others just

stainless steel flex conduit. Additionally, only certain

components were specified for weep holes.

  • Page 49 section 4.1 Installation requirements indicates that the

conduit seal may not be necessary for those limit switches

installed in the Reactor Building. This requirement should be

clear and should specifically list those limit switches which

require conduit selling to ensure qualification.

  • Page 13 lists the 16 Namco EA180 limit switches which had been

installed. However only 14 were considered qualifieo by this ODP.

Unit I limit switch tag numbers 1821-ZS-5373 and 1B21-ZS-5374 were

excluded from the E0 requirements by ESR-97-00431. The Unit 2

equivalent switches were not discussed in the ODP.

. _ _ _ _ .

. _ _ _ _ _ _ _ _ _ - _

,

25

  • In Section 2 of the 00P it was stated that it was a good

maintenance practice to lubricate the NAMCO limit switches.

however. lubrication was not specified in Section 4 of the ODP

which lists recommended maintenance practices.

In Section 4.2 of the ODP it was stated that the switches can be

refurbished. However, a statement was made on page 21 that

qualified replacement part kits were no longer available.

  • A reference was made to abnormal temperatures on page 38 of the

ODP. However, abnormal temperatures were not included in DR 227.

  • The inspectors questioned apparent inconsistencies between

activation energies and aging methods discussed in referenced

qualification test reports (OTRs).

The licensee indicated that these comments would be evaluated by

the E0 group and if appropriate, addressed in Revision 4 of the

QDP when it is completed.

The inspectors reviewed a draft copy of Revision 7 of ODP-67

General Electric Company IC 7700 Series Motor Control Centers for

BNP. The GE MCCs. located or, the 20, 50, and 80 foot elevations

of the Units 1 and 2 Reactor Buildings, are subject to harsh

environments resulting from postulated design basis accidents and  ;

have a safety function to mitigate the consequences of these F

accidents. The MCCs were qualified in ODP-67.

A series of similarity analysis were performed to demonstrate

similarity between the tested configuration and supplied. The

inspectors reviewed portions of DR 232. "Nutherm Report No. CPL-

7806R. Qualification Test Results Applicable to Brunswick Nuclear

Power Plant Safety-Related GE 7700 MCCs." Revision 0, dated

June 30, 1997 which dccumented the similarity analysis. Section 2 of

DR-232 contains a discussion on the similarity analysis between the

components tested by NUTHERM and those installed in the Brunswick MCCs.

The similarity discussion covers fuses, stab assemblies, control

transformers control and power wiring, overload heaters. overload

relays, terminal boards, starters and contactors, molded case circuit

breakers. circuit protectors. disconnect switches. potentiometers, and

indicating lights. The similarity analyses were based on the similarity

analyses contained in DR 1.1. GE Company NEDC-30696-P. May 1985. MCC

Oualification Test Report Phase Il for CP&L Brunswick Plant, or were

devices which could be directly linked to a test specimen and did not

require a similarity analysis. Based on review of DR-232 NRC concluded

that NOTHERM was able to establish that the com3onents they tested were

in the same family as those provided by GE in t1e MCCs. This review was

also dccumented in IR 50-325(324)/97-09.

A draft copy of Revision 0 of ODP 99. R. G. Laurence Series 500

and 600 Solenoid Valves was reviewed. The inspectors verified

that similarity analysis was included in the ODPs.

>

+

_ ___ __ ___ - __ _ _ -.

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26

3) Review of EO Walkdown Data

The inspectors reviewed E0 walkdown data which document inspection

of E0 equipment-in the Unit 2 MSIV pit and drywell, and Unit 2

reactor building. Tha E0 walkdowns were performed in accordance

with CP&L Special Procedure OSP-96-014. EQ Equipment Field

Verification. The pyrpose of the walkdowns was to verify the

accuracy of the manulacturer/model number listed in the licensee's

data bases and to verify the equipment installed orientation and

configuration were in accordance with the E0 qualification

documentation. The ins)ectors reviewed walkdown records for scram '

pilot' solenoid valves, 1AMC0 limit switches, temperature elements,

excess flow check valves, and pressure switches. The walkdown

data was recorded on field inspection data sheets which were'then

converted into an electronic data base. The inspectors verified

that discrepancies identified during the walkdowns were documented

either on a work request (WR/J0) for repair, or in a condition

re) ort (CR). The ins)ectors reviewed completed WR/JO numbers 97-

AF JR1, 97-AFUR2, 97- A UR3, and 97-AFUR4. These WR/J0s document

drilling of weepholes in junction boxes in the Unit 2 MSIV pit to

resolve a moisture intrusion issue. These boxes are associated

.

with limit switches for the Unit 2 main steam isolation valves.

L The completed WR/J0s showed that the weepholes were drilled to

resolve the concerns. The inspectors did not identify any

discrepancies in the records reviewed.

4) Review of Environmental Qualification Condition Reports

The inspectors reviewed the licensee's corrective c.,ctions to

L disposition the CRs listed below. These CRs were initiated by the

licensee to-document and disposition nonconforming items whicn

were identified during the ongoing E0 reconstitution project. The

nonconforming items were identified as a result of E0 equipment

walk h ns, review cnd updating of E0 equipment ODPs, omissions

from the original program, or changes to the operating

environment. The CRs reviewed were as follows:

CR 97-02015

The licensee initiated CR 97-02015 on June 6. 1997 to document and

disposition deficiencies that had been identified by the

licensee's training staff during observation of simulator training

when the fire protection system had not been isolated within the

15 minute time period after initiation of a HELB specified in

31 ant o)erating 3rocedures. The 15 minute time period is the

) asis w1ich esta)lished flood '.evels for E0 e

and north and south RHR and core spray rooms.quipment in the HPCI

Review of closure

for CR 97-02015 disclosed that the licensee concluded that the

issue has been adequately addressed by operator training,

primarily through critiques which were held following the

completion of the simulator training to discuss deficiencies noted

during the training. In response to the CR. Action Items were

Y

_ _ _ _ _ _ _ _

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1

27

'

assigned to the Operator Training group to incorporate the basis

,

for the need to isolate the fire protection system into training

materials. However, review of the training records on June 12,

1997, by personnel from the E0 group resulted in additional

questions regarding the licensee s corrective actions. The

records reviewed by the E0 personnel indicated that during

'

simulator training, approximately 10 to 20 percent of the

operators were failing to enter AOP-05,0, Radioactive Spills. High

. Radiation, and Airborne Activity, or were entering the AOP late

(after 15 minutes). The inspectors made an indepen6nt review of

, the training records reviewed by the E0 personnel. This review

disclosed that the records the E0 personnel reviewed on June 12,

1997 were for the six month

02015 (January - June 1997) The .

period prior to reviewed

inspectors initiation of CR 97-

training

records for July - September, 1997 and noted significant

improvement in this area, although the HELB scenario was not

included as part of the simulator training exercises in this time

period. The training scenario did include a torus leak which

required entry into A0P-05.0.

I

The inspectors noted that the concern regarding flooding of

_

instruments could also be caused by other accidents such as pipe

L breaks in the service water or Reactor Building Closed Cooling

l Water (RBCCW). Operator actions in these cases would be directed

e by E0P-03 SCCP Secondary Containment Control Proccdure (SCCP),

based on high water leve'is in the HPCI and north and south RHR and

core spray rooms. An uttry into E0P-03-SCCP would also result

from flooding in these same rooms caused by activation of the fire

protection system. As aaditional followup on this issue, the

inspectors observed simulator training scenarios performed on

December 3 and 17, 1997. Included in the scenario was a RCIC

steam line break (HELB) and activitation of the fire protection

system. Both crews participating in the training scenario

isolated the fire protection system within the 15 minute time

period. The inspectors also questioned some randomly selected

reactor operators regarding the need for entry into A0P-05.0

following a HELB. The operators were cognizant of the basis of

the actions in A0P-05.0 (need and reason for isolating the ' ire

protection s

CR 97-02015.ystem) and were familiar with the problem addrc ses by

The inspectors verified the action items associated with the CR

were completed. CR 97-02015 was closed on December 11. 1997.

CR 97-01841. 97 02025. & 97-02408 These CRs documented various

issues regarding possible effects of moisture on E0 equipment. CR

97-0184) was initiated to document the effect of spray from the

fire protection system on E0 equipment in the reactor building.

The licensee has resolved all the issues associated with this CR

except for drilling of weepholes in junction boxes whicn may be

affected by the water spray. Licensee engineers are currently

- preparing instructions and procedures for completing this work.

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

-

.

28

The problem documented in CR 97-02025 concerned an issue which had

been the subject of IE Circular 79-05. Moisture Leakage in

Stranded Wire Conductors, which was issued by NRC on March 20.

1979. This affects Patel seals which were used to seal some

stranded wire conductors in instrument circuits. CR 97-0?408

documents several other moisture intrusion issues. The immediate

corrective action taken to resolve these issues, as documented in

CR 97-02408 was to hire an outside consultant to address the

issues. The consultant has reviewed many of the issues documented

in CR numbers 97-01841, 97-02025. and 97-02408 and made

recommendations, some of which have been implemen.ed. The

consultant also addressed another issue in the CRs involving

current leakage in control circuit and the possible impact on ODPs

and E0 of equipment. This concern was the effect of moisture

intrusion through stranded wire conductors, sealed with Patel

seals, which could result in leakage currents in instrument

circuits. ESR 97 00440 was issued for the 120 volt AC circuits and

ESR 97-00441 for DC circuits. These ESRs are currently being

reviewed by licensee engineers. The current leakage issue was

also applicable to questions raised regarding the NAMCO limit

switches. The inspectors will review the licensee's evaluation of

current leakage and its ap311 cation to evaluation of E0 equipment

in a future inspection. T11s was identified to the licensee as

IFl 50 325(324)/97-13-07. Review Technical Evaluation of Current

!

Leakage and the Effect on EQ Equipment. pending further review by

NRC.

The licensee also aerformed an evaluation of the potential for

moisture wicking t1 rough Patel seals. This evaluation was

i documented in ESR 97-00423. 03erability Evaluation - Wicking.

Review of the ESR disclosed t.at the licensee performed a detailed

evaluation of the Patel seals by comparison of the installations

at Brunswick with the configurations tested by NRC at Sandia

Laboratorics (NUREG/CR 0699. Jublished March.1979). The

licensee's conclusions were t1at the design function of the

instellea equipment will not be effected by moisture intrusion

through the stranded wire. The ESR was based on a review of the

duration of the design accidents and the resulting leakage

currents caused by moisture intrusion into limit switches.

Further review of this ESR will be performed as part of IFI 50-325

(324)/97-13-07, discussed above.

CR 97-02016 & 97-02074

CR numbers 97 02016 & 97-02074 were initiated to document issues

involving NAMCO limit switches. The following issues were

identified in the CRs:

  • Inability to identify the date of manufacture of the switches

since the codes for date of manufacture were painted over.

__ ________ ____

__ _ _

I

29

  • Potential for paint to impair the operability of the switches.

The concern was that paint on the roller arms would impair

mechanical function of the switches.

'

  • Chemical reaction between paint and internal switch components

would cause corrosion of switches, leading to failure of the

switches.

  • Use of incorrect qualification test reports (0TRs) in the

qualification test reports which qualified the switches.

  • Effect of current leakage on switch operability.

A total of 14 NAMCO limit switches were covered under the E0

program. These switches were installed during modifications

completed in 1983 and 1984 The licensee has determined that none

of the switches were purchased or manufactured prior to 1980.

Therefore, the concern raised by IE Bulletin 79-28. Possible

Malfunction of NAMC0 Model EA 180 Limit Switches at Elevated

Temperatures, would not apply to the switches installed at

Brunswick, Review of the licensee's response to IEB 79-28

disclosed that none of the potentially defective switches had been

purchased by the Brunswick site.

Review of the i1censee's corrective actions completed to date

disclosed that the following actions have been completed:

The licensee has identified the date of manufacture for most of

the NAMCO limit switches. Additional manufacture dates may be

identified when the Unit 1 walkdowns are completed during the

Spring 1998 refueling outage. However, the licensee has

conclusively determined that none of the switches would be

affected by the defects identified in IEB 79-28.

.

The switches were stroked in accordance with frequencies per the

Technical Specifications which demonstrates that the mechanical

function of the switches had not been impaired by the paint.

  • The paint has been tested. The test results show the

not cause corrosion or deterioration of the switches paint would

. The ODP. has been revised to incorporate the correct OTRs. The

ODP. ODP 49, was still in draft.

. The current leakage issue has been evaluated " ESR numbers 97-

00440 and 97-00441, which are currently being reviewed by licensee

engineers.

The licensee subsequently has determined that the switches were

still within their qualified ;'fe. No equiament operability

issues related to tv.e NAMCO ilmit switches lave been identified.

_

.

30

[R 97 02367

This CR was initiated on July 3, 1997 to document the failure to

initiate CRs for nonconforming items, specifically, MCC door

gaskets and non standard Raychem splices identified as a

violation by NRC during an inspection documented in NRC 1R 50-325

(324)/97 08.- The licensee's corrective actions included

completion of a review of all the E0 walkdown data sheets to

identify any nonconforming equipment. Additional corrective

actions included training of personnel in the E0 group regarding

the corrective action program and assessment of the effectiveness

of the corrective actions. These correcthe actions were also

associated with other similar corrective action CRs. such as CR

97 01972 and CR 97-02465. The inspectors reviewed the completed

corrective actions and concurred with closure of CR 97 02367. The

CR was closed on December 14. 1997.

CR 97-02465 and 97-02672

This CR wac initiated on July 15, 1997, to document concerns on EQ

operability determinations. This CR referenced CR numbers 97-

01841, 97 02025. and 97 02408. discussed above, which involve

moisture intrusion issues. As a result of the concerns raised in

CR 97 02465, the E0 group presented an action plan to resolve the

moisture intrusion issues (CR 97 02465) to the plant nuclear

safety committee. Although, further review showed the operability

determinations for the three CRs were correct, the root cause

analysis concluded that there were other problems which resulted

in CR 97-02465.

The root cause of CR 97-02465 was attributed-to weak E0 project

management. The root cause/ event review for the CR listed the

causal-factors indicative of weak E0 3roject management to be poor

communications within the E0 group, tie site position that E0

problems were primarily docunitation problems, and a poor

corrective action culture within the E0 group. The poor

corrective action culture was evidenced by corrective action items

which were routinely extended, overdue, or completed late: failure

to prepare JCOs: numerous CRs written against the E0 grou) for

improper corrective actions: and closing CR action items )y other

action items without completing the corrective actions. A

violation of NRC requirements was identified in IR 50 325, 324/97-

12 for failure of the licensee to implement their corrective

action program.

The licensee's corrective actions to address the issues raised in

CR 97-02465 included increased management oversight aerforming a

review of the E0 project schedule to complete the higlest priority

work activities first, conducting more frequent E0 group meetings

to improve communications within the E0 group, transferring some

E0 group functions from the Design Control l%1t to a site

organization. and performance of an effer' ve. dss review of the

.

.

.

31

completed corrective actions. The CR was closed on December 17,

1997. The inspectors reviewed the completed corrective actions

.and concurred with closure of the CR. The ins)ectors concurred

with the licensee's conclusions that the opera]ility

determinations for the three referenced CRs were appropriate. NRC

will perform review of the liccasee's actions to correct the l

violation in future inspections,

CR 97-02672, which was inniated on August 5. 1997, indicated that

the Supervisor comments listed in CR 97 02465 were a misstatement

of the consensus of opinion of individuals which met to discuss CR

97-02465. Review of CR 97-02672 disclosed that the CR did not

raise any new issues or conceriis which had not been addressed by

CR 97 02465. CR 97-02672 was closed on December 17, 1997. NRC

concurs with the licensee's conclusions and closure of the CR.

CR 97 4059

This CR was initiated on December 2, 1997, to document concerns

and questions on ESR 97-00426. The questions involved

appropriateness of E0P actions, the need to include evaluation of

drywell instrumentation in tic ESR, and various questions on

instrument setpoints. The 1 Lensee completed a review of the

questions raised in the CR and concluded that the ESR had

addressed these issues, or the issues were beyond the scope of the

ESR, For exam)le, appropriateness of E0P actions were approved by

NRC for all BW1s and do not involve instrument setpoints. There

are no instruments in the drywell which provide signals for

automatic actuation. The inspectors reviewed the licensee's

responses to the questions in the CR and concurred with the

licensee's conclusions that no new corrective actions were

required to resolve the concerns / questions raised in CR 97-04059-

which had not been previously resolved.

5) Review of Environmental Qualification Requirements in

Procurement Practices

Th'e inspectors reviewed CP&L procedure MCP-NGGC-0401, Material

Acquisition (Procurement. Receiving, and Shipping). Revision 4,

dated August 26, 1997. This procedure specifies the instructions

for procurement of safety related materials for use in CP&L

nuclear plant. The inspectors noted that the requirements for

obtaining reviews by E0 engineers is specified in the procedure.

Discussions with licensee engineers and review of previous

revisions of the procedure disclosed that the procedure had been

revised to strengthen the need for the E0 review in Revision 2 of

.MCP-NGGC 0401, effective April 15. 1997. Revision 2 added

- - - - -

requirements that components that require environmental

qualification:be reviewed by the E0 group.

During review of CRs. the inspectors identified several examples

of acceptance of materials / equipment by procurement engineering

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

.

32

for use in E0 installations which were based on test reports which  ;

had not been reviewed by the E0 group -These were documented in

'CR numbers 97-01970 and 97-03036, Several additional examples of

discrepancies in documents prepared by procurement engineering

which affected E0 equipment were also identified during review of

procurement specifications and other documents su * as material

evaluations. These discrepancies were documented in CR 97-04035

which tas initiated on November 25, 1997. The review of

procurement documents was being performed as part of the

corrective actions to address the E0 program discrepancies

identified in IR 50-325(324)/96 14. This was listed as Commitment *

  1. 4 in the licensee's December 19, 1996 Reply to Notice of ,

Violation,

6) Equipment Lubrication Requirements

The inspectors reviewed CP&L procedure MMM-053. Equipment

Lubrication Application Guidance and Lubricant Listing,

Revision 6 dated November 11, 1997. This procedure provides a

listing of plant equipment with recommended lubricants to be used,

guidelines for lubrication of plant equipment, and lubricant

sampling methods. The inspectors identified the following issues

after reviewing the procedure:

-

ODPs 26, 68, and 88 were not referenced in procedure MMM-

053. These ODPs cover environmental qualification of

Reliance electric motors.

- Document References corresponding to above ODPs were not

referenced.

- The types of lubricant specified fo, the Reliance motors in

procedure MMM 053 differ from those listed in the ODPs 26

and 68.

-

Procedure MMM 053 permits maintenance to change the

lubricant without obtaining engineering review or approval.

Discussions with licensee engineers disclosed the CR 97-04015 was

initiated on November 20, 1997, to document the fact that the

procedure permits changes to lubricants without performance. of an

engineering review. Action Item 40 to CR 97-02627 was issued to

document a similar issue. This action item was closed by CR 97-

04015.

The inspectors determined that the licensee had not evaluated that

the type of lubricants (Mobil) specified-in procedure MMM 053 for

Reliance electric motors differed from those listed in ODP 26 and

68, Review of ODP 26. Revision 1. Joy Fan /Peliance Electric

Company, Class 1E Continuous Duty, 20 HP, and ODP 68, Revision 5.

-Standby Gas Treatment System - Fair Company Filter Unit and

Control, showed that the electric motors were both qualification

_ _ _ _ _ - _ _ _

.

33

'

tested using Chevron SRI 2 grease. The impact of using a

dif ferent type of grease to lubricate the motors on the

environmental qualification testing of the motors had not been

documented by the licensee. The licensee initiated CR 97 04064 to

document the fact that substitution of alternate lubricants had

not been evaluated by E0 engineers. The failure to establish

maintenance procedures appropriate to the circumstances for

performing maintenance was identified to the licensee as another

example of violation item 50 325(324)/97-13-02. Inadequate

Procedure for the Conduct of E0 Preventive Maintenance.

c. Conclusions

1

One violation example was identified regarding an inadequate E0

maintenance procedure for lubrication of E0 electric motors. Two

inspector followup items were identified to followu) on revisions

to instrument setpoint procedures and to review leacage current

calculations. The licensee was making progress in resolving and

closing CRt identified by the E0 group. As of the inspection

dates, no 0DPs had been issued.

E5 Engineering staff Knowledge and Qualification

E5.1 Trainino and Qualification of E0 Personnel

a. Insnection Scone (37550)

The inspector reviewed the licensee's program for training and

qualification of personnel in the E0 task force. including both

CP&L and contract engineers,

b. Observations and Findinos

The requirements for performance of E0 equipment walkdowns are

specified in CP&L Special Procedure OSP-96-014. E0 Equipment Field

Verification. The prerequisite in procedure OSP 96-014 for

individuals performing the walkdowns was to read the procedure.

The licensee qualified a number of individuals to perform the

field walkdowns through a training program conducted in accordance

with CP&L procedure TI-100. Conduct of Training. These

individuals included Instrumentation and Control technicians.

contract engineers, and personnel assigned to the E0 group who

were qualified E0 engineers. The training for the qualified E0

engineers consisted of reading the procedure. orientation and on-

the-job training to become familiar with the walkdown and data

s gathering process. For other personnel, the training included

reading of the procedures, formal classroom lectures.

demonstrations, performance of practical exercises, and on-the-job

training. The walkdown group supervisor performed a detailed

review of the result < of practical exercises and data gathered <

during initial walke is prior to signifying the individuals were

s. _ __

34

qualified to perform walkdowns. The training provided for the

walkdcwn personnel exceeded the procedural requirements. The E0

walkdown grou) supervisor stated that the level of training

provided to t1e walkdown personnel war to assure that the walkdown

results were very accurate and to preclude the need for repeat

work. The inspectors revieweJ the training records for the

walkdown personnel and verified that they had been trained in

accordance with the licensee's program. The inspectors noted that

the experience level for the walkdown personnel varied from a

recent graduate engineer to individuals with more than 20 years of

experience. The inspectors reviewed the walkdown inspection

records prepared by various individuals in the walkdown group and

noted that the original walkdown records were complete and

accurate, with some exceptions. Discussions with the walkdown

group supervisor disclosed that corrections noted on the records

were the result of reviews perfnrmed to resolve discrepancies in

the records. The changes were made as a result of additional

walkdown inspections which were doc'mented in the records. In one

case, an individual was terminated for failure to perform the

walkdowns and complete the walkdown records properly. This

individual's work was reviewed by the licensee and corrected where

necessary.

The inspectors also reviewed the training and qualification

records for E0 technical personnel. These records included

previous work experience, education and training, and CP&L

specific training applicable to the E0 project. This training

included E0 technical reviewer, E0 design verifier E0

calculations, and E0 ESR originator. The inspectors also

questioned the manager of the E0 group concerning work assignments

within the E0 grou). That is, assignment of specific activities

to individuals wit 1 previous experience in a particular area of

specialization, such as review of requirements for qualification

of motors or specific types of instrumentation. The E0 group

manager has recently are)ared a directory of all engineers working

within the E0 group w11c1 lists each engineer's experience and

what work activities they have completed for the E0 project at

Brunswick. The purpose of this directory was for the engineers

within the group to know who has worked on various problems and

issues so they could obtain assistance from these individuals when

they become involved with similar technical issues. The directory

was distributed'to personnel in the E0 group. The E0 group

manager provided a copy of the directory to the inspectors and

discussed the basis for the various work assignments within the

group.which were based on the past work experience of the E0

technical personnel,

c. Conclusions

The inspector concluded that the licensee's program for training

and qualification of E0 engineers meets NRC requirements.

,

.

.

35

E8 Hiscellaneous Engineering Issues (37551, 92903)

E8.1 (Closed) URI 50-325(324)/97-08-04: Control of Ecuioment Data Base

System (EDBS) Information

The licensee issued CR 97-02400. Non Validated EDBS Information,

concerning rc, tine use of non-validated EDBS information. This wes

associated with VIO 50 325(324)/97-08 03. Safety Relay Setting Change

Made as Pen and Ink Changes to Procedure. The licensee replied to this

violation on September 2. 1997. The reply discussed licensee corrective

'

action regarding the use of EDBS. Likewise. the licensee responded on

November 26. 1997 to VIO 50-325/97-11-01. Failure to Initiate Alternate

Safe Shutdown Impairment. addressed corrective action fcr use of an EDBS

non validated field for determination of an Alternate Safe Shutdown

impairment. Plant procedure OENP-33.6. Equipment Data Base System

Control and Revision, provides instructions for control of EDBS

information. Color coding of fields in the electronic database

represent the various types of data present. This procedure provides

direction that certain types of data are not to be used until verified.

Accordingly two previous violations address the use of non-verified

EDBS information. The licensee corrective actions for these violations

are being completed. The requirements for the control of information

are in procedure OENP-33.6. Previous items address the concern of this

URI. therefore this item is closed.

E8.2 (Closed) LER 50-325(324)/97-04: Soent Fuel Shionina Cask Handlina

Activities

This report documented the discovery by the licensee that the heavy load

analysis as described in tne UFSAR did not completely bound movement of

the shiroing cask from the primary lift to the secondary lift with the

valve box covers removed. It was determined that movement of the cask

with a non single failure proof yoke and less than full cask integr'ty

constituted an unreviewed safety question (US0) in accordance with the

requirements specified in 10 CFR Part 50.55 The failure to obtain

prior approval for a previously unanalyzed condition was determined in

IR 50-325(324)/97-12 to be a violation. In a letter to the NRC dated

August 6. 1997, the licensee requested a license amendment for review of

the US" The licensee re evaluated findings relative to the 30 foot

dro: ~cident and qualified the transfer yoke using guidance provided in

NUR b 0612. Control of Heavy Loads at Nuclear Power Plants. This

evaluation contended that a fuel shipping cask drop event was not

credible. therefore operation with less than full cask integrity was no

longer a problem due to acceptable redundancy in the lifting yoke. In a

letter to the licensee dated December 2. 1997, the NRC accepted the

licensee determination that operation with the valve covers removed

would not compromise the health and safety of the public due to

acceotable redundancy of the lift devices. Based on the acceptance by

the NRC of the licensee's evaluation and issuance of the enforcement

action as described in IR 50-325(324)/97-12 this item is closed.

.- . ._

_ _ . . _ _ _ _ _ _ _ . . _ . _ . _ . _ _ _ . _ _ _ _ _ _ _ . _ _ _ . _ _

.

4

36

E8.3 (Closed) Inspector Followun item 50-325(324)/96-14-05.'Effect of EO

Accuracy on Instrument Setooint Calculations.

'

Review of procedures and various documents by an independent *

contJ1 tant had resulted in a number of questions regarding the

~

effect of environmental effects (uncertainties) on instrument

accuracy The questions / concerns were documented in an E mail *

message dated June 20, 1997. subjert E0 and Instrument Accuracy,

in order to address the issues raised in the June 20 E mail

message, a review of instrument setpoint calculations was

performed by licensee instrumentation and controls (l&C)

engineers. . The review was documented in ESR 97-000426, which was

'

discussed in paragraph El.3. above. The inspectors also reviewed

various instrument setpoint calculations (documented in paragraph

"

E1.2. above) and determined that E0 accuracy has been aroperly

considered in the instrument setpoint calculations. T1e

ins)ectors had no further questions regarding instrument setpoint

metloaology or accuracy at this time.

E8.4 JClosed) Violation item 50-325(324)/97-02-08. Failure to Imolement ao

nsoection Procram for Safety-Related Miscellaneous Structural Steel

The licensee responded to this violation in letters dated

April 30. 1997, and June 26. 1997 Subject: Reply to Notice of

Violation. The licensee's corrective actions included revision of

Specification 248-107 and review of other specifications to assure OC

inspection criteria required by applicable codes and standards

referenced in the UFSAR had been included in the specifications.

Specifications reviewed included the following: 248-117 - Installation

of Piping Systems: 048 012 - Installation of Electrical Cables: 006 001

- Design. Testing & Inspection of Concrete Mixes. Concrete Materials and

High-Strength Bolts: 005-005 - Design. Testing, & Inspection of Concrete

Mixes. Concrete Materials: 013 001 - Concrete Work: and 018-002.

Miscellaneous Steel. Additional corrective actions included inspection

of a sample of safety related high strength bolts installed using

Specification 248-107. The inspectors reviewed the results of the

structural steel inspectior.s which were documented in ESR 97-00085.

-

hiscellaneous Structural Steel Connection Inspections. The licensee

also revised procedure MMP-013. to incorporate the specification 248-107

changes and trained OC. engineering and planning personnel on the

changes to specification 248-107 which now require additional QC

inspections. The inspectors reviewed records which documented

inspections performed for selected USl A-46 modifications completcd on

Unit 1 during the Fall.1997 refueling outage and verified the

structural steel inspections were completed in accordance with the

revised procedures.

4

Ee.5 (Closed) Violation item 50-325(324)/97 08-07. Failure to initiate

Condition Reports to [,0cument Nonconformina E0 Items

I

. The licensee

September 2. 199 reshonded

Subject: Reply to this violation

to Notice of Violation. in a letter The dated

,

_ _ , _ . - . . _ . _ , . . . _ _ - , . - _ - -_ __,

37

licensee's corrective actions included training of E0 personnel on

the corrective action program, a review of che E0 walkdown data

sheets to identify any potential nonconforming conditions which

had not been previously identified and dispositioned, and

organizational changes to improve management o"ersight in the E0

group. CR 97-02367 was initiated by the licensee on July 3. 1997

to document and disposition the two s)ecific examples of failure

to initiate CRs identified by NRC. Tie inspectors ceviewed the CR

closecut records (CR was closed on December 14, 1997) and the

licensee's corrective actions and verified that the actions were

completed in accordance with the licensee's violation response.

IV. Plant SuppEt

R1 Radiological Protection and Chemistry Controls

RI.1 Use of locks to Control Access

a. Insnection Stone (71750)

The inspector verified a selected sampling of doors required to be

locked, by plant TSs and procedures, fc r the purpose of radiation

protection,

b. Observations and Findinas

The inspector reviewed Environmental & Radiological Control 0E&RC-0040.

Control of Locked High Radiation and Very High Radiation Areas, to

determine the controls used to lock high radiation area doors and

barriers. The inspector located a sampling of the locked high radiation

area doors specified in OE&RC-0040 and tested them to ensure that they

were locked. The ins)ector found that all the locked high radiation

doors tested were locced,

c. Conclusions

The ins)ector determined that each of the locked high radiation area

dcors w11ch were checked were locked. The ins)ector concluded that the

licensee is satisfactorily controll1ng locked ligh radiation areas in

the plant.

R1.2 Radioactive Material Controls

a. insoection Scqoe (71750)

The inspector conducted a housekeeping tour of radioactive material

storage areas located in outside areas within the protected area,

b, Observations and Findinas

The inspector found several poor radiological work practices in the

radiological material (RAM) storage area located aojacent to the

_ _ _ - - _ . _ _ _ _ _ . - _ - . - _ _ . _ _ _ _ _ - _ _ _ _ _ . . _ _ _ _ . _ .

.

38

Radiological Maintenance Service Building in the northwest corner of the

p.*otected area. A bucket containing scaffolding brackets was half

filled with water and was labeled as radioactive material. The label

identified the brackets as contaminated. This practice had the

possibility of allowing the potentially contaminated water to cause a

spread of contamination in an RAM storage area. There was also

scaffolding identified as radioactive lying unprotected on a wooden

pa l l e'. .

The ~icensee conducted a walkdown of this area and the radiological

service building, and identified multiple conditions requiring action.

These items were identified in CR 97-04122. Nonconforming Material

Condition,

c. Conclusions

The inspector determined that several poor radiological work practices

existed in a radioactive material storage area.

S2 Status of Security Facilities and Equipment

c2.1 Plant Access Control and Physical Barriers

a. Inspection Scone (71750)

The inspector verified the status and condition of the protected area

fencing,

b. Qbser"ations Jnd Findinas

The inspector performed a walkdown of the protected area fence. The

fence was inspected for integrity such as corrosion on the posts, gaps

in the fence, and general adequacy. The inepector noted no

deficiencies,

c. Conclusions

The inspector found the status and condition of the protected area fence

to be satisfactory.

F1 Control of Fire Protection Activities

F1.1 Operability of Fire Protection Facilities and Eauioment

a. Ipsoection Scone (64704)

The inspector reviewed the operation's fire protection daily impairment

reports on the facility's fire protection systems and features, and

inspected these items to determine the performance trends and the

material conditions of this equipment.

.__ _ _ __.- _ _ _ _ _ _.__._ _ _ _ _ . . _ - -

_

4

4

.

'

39 ,

b. - Observations end Findinas  !

A review of the Loss Prevention Unit daily Impairment Reports for

-December 8 - 11, 1997.- indicated that the following fire-protection

,

components or systems for safety related areas were out of service: ,

.

'

fire Protection-System ~ Number of Imoairments

Thermo-Lag Fire Barriers 2

Fire Doors 6

'

, Cable Coating- 1

-

Fire: Detection System - 3 1

Fire Suppression System 3

The inspector noted that a number of- fire doors were out of service.

This high number was attributed to the current DG building fire door

corrective action (door replacement and repairs) that was in process for

discrepancies identified during a June 1997 licensee self assessment of

the fire protection program.- Appropriate compensatory measures had been

-

-1mplemented for the fire protection features which were out of service.

The impairment status report provided the licensee with a good means of

identifying out-of-service fire protection equipment and provided status

-

for compensatory measures that were implemented. The corrective

maintenance on degraded fire protection systems was accomplished in a

-

timely manner,

,

During the plant tours the inspector noted that the maintenance and

material condition of the fire protection equipment were satisfactory.

c. Conclusions

'

Correstive maintenance on degraded fire protection systems was

accomplished in a. timely manner.>The maintenance and material condition

,

of the fire protection equipment and features were satisfactory.

-

,

F2 Status of Fire Protection Facilities and Equipment

F2.1 E3ssive Fire Barriers

.

Fire barriers ~ include penetration seals. wraps, walls. structural member--

fire resistanticoatings.. doors, dampers. etc. Fire barriers are used to

-prevent the spread of fire and to protect redundant safe shutdown

equipment. Laboratory testing of fire barrier materials is done only on

a-limited range of test assemblies. In-)lant-installations can vary

-,

from the tested configurations. -Under tie provisions of Generic Letter

(GL) 86-10. Implementation of Fire Protection Requirements, licensees

are permitted to develop engineering evaluations justifying such

deviations.

w -, ,, - . . . -. - - . - - ,. . -

. . _ _ _ _ _ - _ - _ _ - _ _ _ _ _ _ _ _ _ .

'

40

2.2 Silicone foam Penetration Seals

a. Inspection Stone (64704)

The inspector reviewed the fire barrier ,,ilicone foam penetration seal

design end testing. The inspector compared as-built fire barrier

silicone foam penetratioh seals to fire endurance test configurations to

verify that the as-built penetration seals reviewed were qualified by

appropriate fire endurance tests, representative of, and bounded by, the

design and construction of the fire endurance test specimens. During

plant walkdowns the inspector observed the installation configurations

of selected fire barrier silicone foam 3enetration seals to unfirm that

the licensee had established an accepta)le design basis for those fire

barriers used to separate safe shutdown functions.

b. Observations and Findinas

The inspector reviewed the fire barrier seal design and testing for six

of ten fire barrier silicone foam seal penetrations, Additional reviews

I are documented in NRC 1Rs 50-325(324)/92-31, 93 08. and 93-38.

The inspector reviewed Brunswick Specification No. 118 003, Revision 7.

Selection and Installation of Fire Barrier Penetration Seals: Corrective

Maintenance Procedure OCMP-010, Revision 2, Installation of Fire

Barrier, Pressure Boundary Penetration and Water / Moisture Seals: Fire

Protection Procedure FFP-015. Revision 23, Fire Barrier Penetration Seal

Work Control: Periodic Test OPT-34.6.7.12. Revision 3. Fire Barrier

Penetration Seals: and the Fire Hazards Analysis (FHA) for the location

and description of fire areas: and assessed the licensee's supporting

technical justification and any available engineering evaluations for

the sampled silicone foam type oenetration seals,

The inspector's review focused on verifying that the following design

and installation paramaters for the as-built configurations were

adequately bounded and justified by the licensee's engineering

evaluations:

. penetration opening sizes

e thermal mass of penetrating items

e clearances of penetrating items

e unexposed surface temperatures

The insoector found that penetration seal field verification

documentation was maintained by the licensee. However, the seal

installers * qualification and training records were not readily

available for review. Although the installation and repair procedures

for penetration seals provided adequate guidance to ensure materials

were installed per design requirements, the inspector could not verify

that the established surveillance recuirements included vendor

recommendations for inspection and icentification of silicone foam seal

aging and shrinkage.

- - - - - - _ _ _ - - - _ - - . - - - . - - - - - - - . . - -

'

.  :

41

The licensee was unable to locate the penetration seal testing

documentation and the vtador data for the tested prototype

configurations or GL 8610 engineering evaluation documentation that

evahated the adequacy of the deviations from a tested fire barrier

contiguration. This does not satisfy the guidar.ce of GL 8610. The

i

licensee stated that industry documentation is available to support

silicone foam penetration seal installations at Brunswick but the

.tiformation was maintained at other Carolina Power and Light (CP&L)

sites.

The penetration seal testing documentation, vendor data and inspection

criteria, installer qualification and training records, and evaluations

of deviations from tested fire barrier configurations will be reviewed

during a subsequent NRC inspection. This is identified as IFl 50 325

(324)/97-13 04. Review of Licensee Records and Engineering Evaluations

to Establish the Fire Resistant Capabilities of Fire Rated Silicone foam

Penetration Seals,

c. Conclusions

The inspector concluded that silicone foam penetration seal field

verification documentation was maintained by the licensee. The

installation and repair procedures for penetration seals provided

adequate guidance to ensure that materials were installed per design

requirements. However, the designs were not supported by seal testing

documentation, vendor data and inspection criteria, installer

qualification and training records, and engineering evaluations that

satisfy the guidance of GL 8610 for deviations from the fire barrier

configuration qualified by tests.

F2.3 Fire Doors

a. Insnection Scone (64704)

The inspector reviewed UFSAR Section 9.5.1.4.3.4.b. Fire Doors, and

performed plant walkdowns to verify that the UFSAR wording was

consistent with the observed plant installation configurations for

selected fire doors installed in fire barriers used to separate safe

shutdown functions.

b. Observations and Findinas

The UFSAR St.ction 9.5.1.4.3.4.b. Fire Doors, states that doors and

frames are either listed by a national testing laboratory or are

constructed similar to listed doors and frames. All doors and frames

have been evaluated to assure satisfactory ratings. Results are

documented in the FHA. During the review of the FHA the inspector

identified that, while evaluations of fire doors and frames existed. the

-licensee failed to document their results in the FHA. which is section

9.5.1.5 of the UFSAR.

1

- - , r ,,- ~ , - , , - , , - , - - - - - - - , -v ,

_ _ _ _ _ _ - _

42

After discussions with the licensee. CR 97-04103 was issued to track the

l failure to provide the results of fire door evaluations in the FHA.

This UFSAR discrepancy was identified by the inspector and is discussed

in Section F2.4.

A review of the surveillance ins)ection and testing procedures for fire

doors was performed to confirm tlat the licensee specified fire door

clearance acce)tance criteria was in accordance with the guidance of

National Fire )rotection Association (NFPA) 80. Standard for Fire Doors

and Fire Windows. On December 10. 1997. the inspector observed ongoing

door replacement and repair activities for fire doors in the DG

building. No discrepancies were identified,

c. Conclusions

I

The inspector concluded that fire door surveillance prc:edures and

acceptance criteria for verification o' fire daor clearances were in

accordance with NFPA quidance. Howevr a UFSAR discrepancy associated

documentation of fire door and frame eu.uations was identified.

F2.4 UFSAR Review

A recent discovery of a licensee o)erating the facility in a manner

contrary to the UFSAR description lighlighted the need for a special

focused review that compares plant practices, procedures, and/or

parameters to the UFSAR descriptions. While performing the inspections

discussed in this report. the inspector reviewed the applicable portions

of the UFSAR that related to the areas inspected. The inspector

verified that the UFSAR wording was consistent with the observed plant

practices, procedures, and/or parameters.

The inspector reviewed UFSAR Section 9.5.1.4.3.4.b, Fire Doors, as part

of the fire protection program review activiti u , An inconsistency was

noted in that the licensee failed to document the results of evaluations

of fire doors and frames in the FHA which is section 9.5.1.5 of the

UFSAR. This issue is discussed in Section F2.3. This item will be

identified as part of URI 50-325(324)/97-13-05. UFSAR Discrepancy Fire

Doors.

F3 Fire Protection Procedures and Documentation

F3.1 Fire Protection Procedures

a. Insoection Scone (64704)

The inspector evaluated the adequacy and implementation of the

licensee s Eire Protection Program described in the UFSAR and in Plant

Operating Manual Fire Protection Procedure OPLP 01. Revision 6. Fire

Protection Program Document. In addition a comparison was made of the

program to selected NRC Safety Evaluation Reports which ap3 roved the

station fire protection program. The inspector reviewed t7e following

>

procedures for compliance with the NRC requirements and guidelines:

.

. . . . - .. ~ .

..

.

.

. _ . . . . .

.

.

.

.

.

43

-

OPLP-01. Revision 6. Fire Protection Program Document

-

0FLP-01.1. Revision 12. Fire Protection Commitment Document

-

OPLP-01.2 Revision 10. Fire Protection System Operability.

Action, and Surveillance Requirements

-

FPP 005. Revision 15. Fire Watch Program

-

FPP-008. Revision 24. Fire Protection Weekly inspection

-

FPP 013. Revision 25. Transient Fire Load Evaluation

-

FPP 014. Revision 17. Control of Combustible. Transient Fire loads

!

and Ignition Sources

Plant tours were also performed to assess procedure complianc.e.

b. Obji.ervations and Findinas

The listed procedures were issued to implement the facility's fire

protection program. These procedures contained requirements for program

administration, controls over combust 1 oles arid ignition sources, fire

watch duties and training, and operability requirements for fire

i

protection systems and features. The 3rocedures were well written and

met the licensee's commitments to the 1RC.

General plant walkdown inspections were perfoimed by the inspector to

verify: acceptable housekeeping; compliance with the ]lant's fire

prevention procedures such as control of transient com)ustibles:

operability of the fire detection and suppression systems: emergency '

lighting: and installation and operability of fire barriers, fire stop

and penetration seals (fire doors, dampers, electrical penetration

seals, etc.),

c. Conclusions

General housekeeping was satisfactory. Fire retardant plastic sheeting

and film materials were being used. Lubricants and oils were properly

stored in approved safety containers. Controls for combustible gas bulk

storage and cutting and welding operations were being enforced.

Controls were being properly maintained for limiting t' alsient

combustibles in designated separation zones and oth' restricted plant

. areas.

F5 Fire Protection Staff Training and Qualification

F5.1 EireBrioade

a. Insoection Stone (64704)

,

,-- _____.

_ _ _ _ _ _ . _ - . _ . _ _ _ _ _ . _ _ _ _ _ - - _ _ . - . . _ _ _ _ _ _ __

m

. 1

1

44

The inspector reviewed the fire brigade organization and training

program for compliance with the NRC guidelines and program requirements.

'

b. Observations and Findinos

'

The organization and training requirements for the plant fire brigade

were established by Fire Protection Procedure 0FPP-051. Loss Prevention

Emergency Response 0ualification/ Training and Drill Program. The fire

brigade for each of five shifts was composed of an operations support

fire protection technician shift incident commander (fire brigade

leader) and at least four additional brigade members consisting of

Auxiliary Operators. Chemistry Technicians and Maintenance personnel.

Each operations shift also had a Senior Reactor Operator / Reactor  :

Operator Fire Brigade Advisor assigned to respond tr ' ires with the fire

brigade.

As of the date of this inspection, there were a total of 48 fire brigade

members 26 from operations and 22 from E&RC and Maintenance on the

pic t fire brigade. The inspector verified that sufficient shift

personal were available to staff each shift's fire brigade with at

least five qualified fire brigade members.

A review of the training records for the fire brigade members indicated

that the training, drill, respiratory and physical examination

requirements for each active member were up to date and met the

established site training requirements.

Fire Briaade Ecuioment:

The fire brigade turnout gear and a fire response vehicle and trailer

with fire brigade equi) ment was stored in the Operations / Fire Protection

equipment building. T1e_ inspector's inventory of the fire brigade

equipment indicated that a sufficient number of turnout gear, consisting

of coats, pants, boots, helmets, etc. , was provided to equip the fire

brigade members expected to respond in the event of a fire or other

emergency. The fire brigade turnout i., ear and fire fighting equipment

were being properly maintained,

c. Conclusions

The fire brigade organization and qualification training met the

-requirements of the site procedu.m . Fire brigade turnout gear and fire

fighting eouipment were being properly maintained.

__ .__ -

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..

l

e l

45 j

F6 Fire Protection Organization and Administration

F6.1 Fire Protection Mananement and OraanizatioD

a. Inspection Scope (64704),

The licensee's management and administration of the facility's fire

protection program were reviewed for compliance with the commitments to

the NRC and to current NRC guidelines.

b. Observations and Findinos

During this report period the licensee reassigned the responsibility ior

the administration and implementation of the fire protection program

from the previous Loss Prevention Unit (LPU) to the Operations Shift and

Support organizations. The LPU organization was dissolved.

The designated onsite manager responsible for the administration and

implementation of the fire protection program was the Operations

Manager, This responsibility had been delegated to the Operations

Support Superintendent. The Operations Support Superintendent was

responsible for the station fire protection program, fire protection

surveillance testing of fire protection systems and equipment, and

ensuring that the aopropriate fire prevention procedures and fire

b:'igade programs were implemented. A Fire Protection Program

C0ordinator reported to the Operations Support Superintendent.

Maintenarice of the 31 ant fire protection equipment was performed by the

Maintenance Unit. cire protection related training was planned and

conducted by the Brunswick Training Se: tion. Coordination of the

station's fire protection program commitments and engineering functions

was provided by a fire protection system engineer in the Brunswick

Engineering Support Section,

c. Conclusions

The coordination and oversight of the facility's fire protection program

had been reassigned from the previous LPU organization to Shift

Operations. The new organizational structure met NRC guidelines and the

licensee's fire protection program requirements.

F7 Quality Assurance in Fire Protection Activities

F7.1 Fire Protection Audits

a. Insoection Scope (64704)

The following audit report and the plant response to the issues were

reviewed:

- Nuclear Assessment Section (NAS) Report B-FP-97-01. Brunswick Fire

Protection and Loss Prevention Unit Assessment, dated

August 1. 1997.

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b. Observations and Findinas

The licensee's Nuclear Assessment Section performed an assessment of the

fire protection program and LPU on June 16-27. 1997. The report for

this assessment was Re) ort No. B FP-97 01. The assessment team

determined that the LPJ fire prevention and fire response activities

were adequate; however, its implementation of the fire protection

)rogram was ineffective based on a number of program elements found to

)e below acceptable standards. Findings from these assessments were

categorized as strengths, issues, or weaknesses. The assessment report

identified six program element issues and one weakness.

The inspector reviewed the final audit report, the licensee's response

to the identified issues. the planned corrective actions, and the NAS

evaluation of the response adequacy.

This NAS assessment of the facility's fire protection program was

comprehensive and effective in identifying fire protection program

performance deficiencies to management. The audit team identified

deficiencies in LPU'c management oversight of fire protection

procedures, training, problem identification, procedure performance

standards, corrective actions, and personriel safety. Corrective actions

in response to the identified issues were substantial and included a

fire protection reorganization to integrate the former LPU organization

into the shift Operations and Operations Sup) ort organizations under

direct management of the Operations Support Manager,

c. Conclusions

The 1997 Nuclear Assessment Section assessment of tite facility's fire

protection program was comprehensive and was effective in identifying

fire protection program performance deficiencies to management. Planned

corrective actions in response to the audit issues were substantial and

included a fire protection reorganization.

V. Manaaetment Meetinas

XI Exit Meeting Summary

The inspector presented the inspection results to members of licensee

management at tN conclusion of the ins)ection on January 8,1998. Post

inspection briefings were conducted on )ecember 12, 1997. The licensee

acknowledged the findings presented. The licensee stated that they had

not determined if clearance records were required QA records.

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PARTIAL LIST OF PERSONS CONTACTED

Licensee

A. Brittain. Manager Security

M. Christinziano, Manager Environmental and Radit lon Control

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W. Dorman. Supervisor Licensing and Regulatory Programs

N. Gannon. Manager Maintenance

J. Gawron. Manager Nuclear Assessment Section

S. Hinnant. Vice President. Brunswick Steam Electric Plant

K. Jury. Manager Regulatory Affairs

R. Krich, Chief Engineer. Nuclear Engineering Department

B. Lindgren. Manager Site Su) port Services

J. Lyash. Manager Brunswick Engineering Support Section

R. Mullis. Manager Operations

Other licensee employees or contractors included office, operation,

maintenance. chemistry, radiation, and corporate personnel.

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INSPECTION PROCEDURES USED

IP 37550: Engineering

IP 37551: Onsite Eng11eering

IP 61726. Surveillance Observations

IP 62700: Maintenance Program implementation

IP 62707: Maintenance Observations

IP 64704: Fire Protection

IP 71707: Plant 0)erations

IP 71714: Freeze )rotection

IP 71750: Plant Support Activities

IP 92700: Onsite Followup of Written Reports of Nonroutine Events at Power

Reactor Facilities

IP 92901: Followup - Operations

IP 92902: Followup - Maintenance

IP 92903: Followup - Engineering

ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

50-325(324)/97-13-01 VIO Failure to Retain TS Required QA Record (Section

07.2)

50 325(324)/97 13-02 VIO Inadequate Procedure for the Conduct of E0

Preventive Maintenance (Section M1.3, El.4.b.6)

50 325/97-13-03 VIO Failure to Note Abnormal TS Surveillance Values

(Section M3.1)

50 325(324)/97-13-04 IFl Review of Licensee Records and Engineering

Evaluations to Establish the Fire Resistant

Capabilities of Fire Rated Silicone foam

Penetration Seals (Section F2.2)

50-325(324)/97-13-05 URI UFSAR Discrepancy Fire Doors (Section F2.4)

50 325(324)/97-13 06 IFl Revisions to Procedure EGR-NGGC-0153 (Section

El.1)

50-325(324)/97-13-07 IFl Review Technical Evaluation of Terminal Block

Current Leakayc and the Effect on EQ Equipment.

(Section El.4.b.4)

Closed

50-325/96-15-01 URI Vessel Disassembly Without Secondary Containment

(Section 08.1)

50-325(324)/97 02-01 V10 Locked Valve Out of Position (Section 08.2)

50-325/97 12 03 URI Recirculation Pump Run back (Section 08.3)

)

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50-325(324)97-12-04 URI Diesel Generator Low Voltage Auto Start Defeated

(Section 08.4)

50 325(324)/96-017-00 LER Invalid Loss of Coolant Accident (Section M8.1)

50_-325/97_009-00 LER Missed Increased Frequency inservice Testing

Requirement (Section M8.2)

50-325/97-001-00 LER Rod Block Monitor Surveillance inadequacy

(Section M8.3)

50-325(324)/95-022 00 LER High Pressure Coolant injection System Discharge

Flow Element Gasket Leak (Section M8.4)

'

50 325/97-05-02 IFl

Abnormal CS Sp)arger Break Detector Indication

(Section Md.5

50 325/97-05-03 VIO Inadequate CS Surveillance Procedure (Section

M8.5)

50 325/97-02 LER Core Spray Header Differential Pressure

Instrumentation Inoperable (Section M8.5)

50-325(324)/97-02-04 VIO Failure to implement Requirements of the

Maintenance Rule (Section M8.6)

50-325(324)/97-08-04 URI Control of EDBS Information (Section E8.1)

50-325(324)/97-04 LER Spent Fuel Shipping Cask Handling Activities

(Section E8.2)

50-325(324)/96-14-05 IFI Effect of EQ Accuracy on Instrument Setpoint

Calculations (Section E8.3)

50-325(324)/97-02-08 VIO Failure to Implement an Inspection Program for

Safety-Related Miscellaneous Structural Steel

(Section E8.4)

50-325(324)/97-08 07 VIO Failure to Initiate Condition Reports to

Document Nonconforming EQ ltems (Section E8.5)

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