ML13128A056

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IR 05000237-13-002, 05000249-13-002; 01/01/2013 - 03/31/2013; Dresden Nuclear Power Station, Units 2 & 3; Adverse Weather Protection and Identification and Resolution of Problem
ML13128A056
Person / Time
Site: Dresden  Constellation icon.png
Issue date: 05/07/2013
From: Reynolds S
Division Reactor Projects III
To: Pacilio M
Exelon Generation Co, Exelon Nuclear
References
EA-13-079 IR-13-002
Download: ML13128A056 (56)


See also: IR 05000237/2013002

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION III

2443 WARRENVILLE ROAD, SUITE 210

LISLE, IL 60532-4352

May 7, 2013

EA-13-079

Mr. Michael J. Pacilio

Senior Vice President, Exelon Generation Company, LLC

President and Chief Nuclear Officer (CNO), Exelon Nuclear

4300 Winfield Road

Warrenville, IL 60555

SUBJECT: DRESDEN NUCLEAR POWER STATION, UNITS 2 AND 3, INTEGRATED

INSPECTION REPORT 05000237/2013002, 05000249/2013002; PRELIMINARY

WHITE FINDING

Dear Mr. Pacilio:

On March 31, 2013, the U.S. Nuclear Regulatory Commission (NRC) completed an integrated

inspection at your Dresden Nuclear Power Station, Units 2 and 3. The enclosed report

documents the results of this inspection, which were discussed on April 8, 2013,

with Mr. D. Czufin, and other members of your staff. Additionally on April 19, 2013, the NRC

discussed with Mr. S. Marik, of your staff, the preliminary White determination for the finding

discussed below.

The inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

This report discusses one NRC-identified finding, concerning the sites external flooding

strategy, which has preliminarily been determined to be a White finding with low to moderate

safety significance that may require additional NRC inspections. Specifically, Dresden

Abnormal Operating Procedure, DOA 0010-04, Floods, did not contain steps directing

operators to maintain reactor vessel inventory during a probable maximum flood event when

a reasonable simulation of this procedure was executed in August 2012.

The finding is not a current safety concern. A licensee procedure, TSG -3, Attachment T,

establishing a pathway for adding make-up water to the reactor coolant system during external

flooding events up to and including the probable maximum flood, was implemented in

November 2012.

This finding with the supporting circumstances and details is documented in the enclosed

inspection report. This finding was assessed based on the best available information, using the

applicable Significance Determination Process. The basis for the NRCs preliminary significance

determination is also described in the enclosed report. This finding is also an apparent violation

of NRC requirements and is being considered for escalated enforcement action in accordance

with the Enforcement Policy, which can be found on the NRCs Web site at

http://www.nrc.gov/about-nrc/regulatory/enforcement/enforce-pol.html.

M. Pacilio -2-

In accordance with NRC Inspection Manual Chapter 0609, we intend to complete our evaluation

using the best available information and issue our final determination of safety significance

within 90 days of the date of this letter. The significance determination process encourages an

open dialogue between the NRC staff and the licensee; however, the dialogue should not

impact the timeliness of the staffs final determination. Before we make a final decision on this

matter, we are providing you with an opportunity (1) to attend a Regulatory Conference where

you can present to the NRC your perspective on the facts and assumptions the NRC used to

arrive at the finding and assess its significance, or (2) submit your position on the finding to the

NRC in writing. If you request a Regulatory Conference, it should be held within 30 days of the

receipt of this letter and we encourage you to submit supporting documentation at least one

week prior to the conference in an effort to make the conference more efficient and effective. If

a Regulatory Conference is held, it will be open for public observation. If you decide to submit

only a written response, such submittal should be sent to the NRC within 30 days of your receipt

of this letter. If you decline to request a Regulatory Conference or submit a written response,

you relinquish your right to appeal the final Significance Determination Process determination, in

that by not doing either, you fail to meet the appeal requirements stated in the Prerequisite and

Limitation sections of Attachment 2 of Inspection Manual Chapter 0609.

Please contact Mr. Jamnes Cameron at 630-829-9833 and in writing within 10 days from the

issue date of this letter to notify the NRC of your intentions. If we have not heard from you

within 10 days, we will continue with our significance determination and enforcement decision.

The final resolution of this matter will be conveyed in separate correspondence.

Because the NRC has not made a final determination in this matter, no Notice of Violation is

being issued for the inspection finding at this time. In addition, please be advised that the

number and characterization of the apparent violation described in the enclosed inspection

report may change as a result of further NRC review.

This report also documents one additional NRC-identified finding of very low safety significance

(Green). This additional finding was determined not to involve a violation of NRC requirements.

If you contest the subject or severity of this Green finding, you should provide a response within

30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear

Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with

a copy to the Regional Administrator, U.S. Nuclear Regulatory Commission - Region III,

2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement,

U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector

Office at the Dresden Nuclear Power Station. In addition, if you disagree with the cross-cutting

aspect assigned to any finding in this report, you should provide a response within 30 days of

the date of this inspection report, with the basis for your disagreement, to the Regional

Administrator, Region III, and the NRC Resident Inspector at the Dresden Nuclear Power

Station.

M. Pacilio -3-

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its

enclosure, and your response (if any) will be available electronically for public inspection in

the NRC Public Document Room or from the Publicly Available Records System (PARS)

component of NRC's Agencywide Document Access and Management System (ADAMS).

ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html

(the Public Electronic Reading Room).

Sincerely,

/RA by Kenneth G. OBrien for/

Steven A. Reynolds, Director

Division of Reactor Projects

Docket Nos. 50-237, 50-249

License Nos. DPR-19 and DPR-25

Enclosure: Inspection Report 05000237/2013002, 05000249/2013002

w/Attachment: Supplemental Information

cc w/encl: Distribution via ListServ

U.S. NUCLEAR REGULATORY COMMISSION

REGION III

Docket Nos: 05000237; 05000249

License Nos: DPR-19 and DPR-25

Report No: 05000237/2013002; 05000249/2013002

Licensee: Exelon Generation Company, LLC

Facility: Dresden Nuclear Power Station, Units 2 and 3

Location: Morris, IL

Dates: January 1 through March 31, 2013

Inspectors: G. Roach, Senior Resident Inspector

D. Meléndez-Colón, Resident Inspector

D. Jones, Reactor Inspector

J. Corujo-Sandín, Reactor Engineer

T. Go, Health Physicist

Approved by: J. Cameron, Chief

Branch 6

Division of Reactor Projects

Enclosure

TABLE OF CONTENTS

SUMMARY OF FINDINGS ......................................................................................................... 1

REPORT DETAILS .................................................................................................................... 3

Summary of Plant Status ........................................................................................................ 3

1. REACTOR SAFETY .................................................................................. 3

1R01 Adverse Weather Protection (71111.01).................................................... 3

1R04 Equipment Alignment (71111.04Q and S) ................................................. 7

1R05 Fire Protection (71111.05) ......................................................................... 8

1R06 Flooding (71111.06) .................................................................................. 9

1R11 Licensed Operator Requalification Program (71111.11) ...........................10

1R12 Maintenance Effectiveness (71111.12) ....................................................11

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13) 12

1R15 Operability Determinations and Functional Assessments (71111.15) .......13

1R18 Plant Modifications (71111.18) .................................................................13

1R19 Post-Maintenance Testing (71111.19) ......................................................14

1R22 Surveillance Testing (71111.22) ...............................................................15

1EP6 Drill Evaluation (71114.06) .......................................................................16

2. RADIATION SAFETY ...............................................................................17

2RS1 Radiological Hazard Assessment and Exposure Controls (71124.01) ......17

2RS6 Radioactive Gaseous and Liquid Effluent Treatment (71124.06) ..............19

4. OTHER ACTIVITIES ................................................................................25

4OA1 Performance Indicator Verification (71151) ..............................................25

4OA2 Identification and Resolution of Problems (71152) ...................................26

4OA3 Follow-Up of Events and Notices of Enforcement Discretion (71153) .......36

4OA5 Other Activities .........................................................................................37

4OA6 Management Meetings .............................................................................38

SUPPLEMENTAL INFORMATION............................................................................................. 1

Key Points of Contact ............................................................................................................. 1

Items Opened, Closed, and Discussed ................................................................................... 2

List of Documents Reviewed .................................................................................................. 3

List of Acronyms Used ...........................................................................................................10

Enclosure

SUMMARY OF FINDINGS

Inspection Report (IR) 05000237/2013002, 05000249/2013002; 01/01/2013 - 03/31/2013;

Dresden Nuclear Power Station, Units 2 & 3; Adverse Weather Protection and Identification and

Resolution of Problems.

This report covers a 3-month period of inspection by resident inspectors and announced

baseline inspections by regional inspectors. Two findings were identified by the inspectors.

One of these findings was considered an apparent violation of NRC regulations. The

significance of inspection findings is indicated by their color (Green, White, Yellow, Red) using

Inspection Manual Chapter (IMC) 0609, Significance Determination Process (SDP), dated

June 2, 2011. Cross-cutting aspects are determined using IMC 0310, Components Within the

Cross Cutting Areas, dated October 28, 2011. Findings for which the SDP does not apply may

be Green or be assigned a severity level after NRC management review. All violations of NRC

requirements are dispositioned in accordance with the NRCs Enforcement Policy dated

January 28, 2013. The NRCs program for overseeing the safe operation of commercial nuclear

power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 4, dated

December 2006.

A. NRC-Identified and Self-Revealed Findings

Cornerstone: Mitigating Systems

Green. The inspectors identified a Finding having very low safety significance for the

failure to include acceptance criteria in a surveillance test for equipment that is the sole

source of make-up water to the isolation condenser and spent fuel pool for both units

during a probable maximum flood (PMF) scenario postulated in the Updated Final Safety

Analysis Report (UFSAR). As described in the Exelon Quality Assurance Manual, the

licensee is committed to the requirements of ANSI/ANS 3.2-1988, which states that

surveillance tests contain or reference acceptance criteria in appropriate design or other

source documents.

The inspectors determined that the failure to include adequate acceptance criteria in a

surveillance test was a performance deficiency warranting a significance evaluation.

The inspectors determined that the finding was more than minor because if left

uncorrected, it could lead to a more significant safety concern. Specifically, without any

acceptance criteria in the surveillance test, the licensee cannot determine whether the

flood pump was able to perform its function as described in the UFSAR and calculation

DRE99-0035. The inspectors completed a Phase 1 significance determination of this

finding and determined that the finding impacted the Mitigating Systems Cornerstone.

The inspectors concluded that the diesel-driven make-up pump would be a mitigating

system in the case of the probable maximum flood. The inspectors answered No to

the question on Exhibit 2 - Mitigating Systems Screening Questions of Appendix A, The

Significance Determination Process for Findings At-Power, of IMC 0609. As a result, the

issue screened as of very low safety significance. Similar issues were identified

previously by the inspectors involving inadequate surveillance test and operating

procedures for the flood pump. Therefore, the inspectors determined that this finding

has a cross-cutting aspect in the area of Problem Identification and Resolution,

Corrective Action Program. (P.1(d)) (Section 1R01.3)

1 Enclosure

Preliminary White: The inspectors identified a finding and an associated Apparent

Violation (AV) of Technical Specification (TS) Section 5.4.1. Technical

Specification 5.4.1 requires, in part, that written procedures be established,

implemented, and maintained covering the following activities: the applicable

procedures recommended in Regulatory Guide (RG) 1.33. Revision 2, Appendix A,

February 1978. RG 1.33. Revision 2, Appendix A, Paragraph 6 addresses Procedures

for Combating Emergencies and Other Significant Events and Item w addresses Acts

of Nature (e.g ., tornado, flood, dam failure, earthquakes). From February 20, 1991, to

November 21, 2012, the licensee failed to establish a procedure addressing all of the

effects of an external flooding scenario on the plant. Specifically, DOA 0010-04,

Floods, did not account for reactor vessel inventory make up during an external

flooding scenario up to and including the probable maximum flood event which could

result in reactor vessel water level lowering below the top of active fuel. This finding

does not represent an immediate safety concern in that the licensee now has

procedures for providing reactor vessel make up water during an external flood scenario

up to and including a PMF event.

The inspectors determined that the licensees failure to consider reactor vessel inventory

make up during an external flooding scenario up to and including the PMF was a

performance deficiency warranting a significance evaluation. The finding was

determined to be more than minor in accordance with Inspection Manual

Chapter (IMC) 0612, Power Reactor Inspection Reports, Appendix B, Issue

Screening, dated September 7, 2012, because it was associated with the Mitigating

Systems Cornerstone attribute of procedure quality and adversely affected the

cornerstone objective to ensure the availability, reliability, and capability of systems that

respond to initiating events to prevent undesirable consequences. A Significance and

Enforcement Review Panel (SERP), using IMC 0609, Appendix M, Significance

Determination Process Using Qualitative Criteria, dated April 12, 2012, preliminarily

determined the finding to be of low to moderate safety significance (White). The

inspectors determined that this finding has a cross-cutting aspect in the area of Problem

Identification and Resolution, Corrective Action Program, Self and Independent

Assessments, since it involves the failure to identify the lack of procedural steps to

address a critical function during a comprehensive self assessment of the flooding

strategy. (P.3(a)) (Section 4OA2)

B. Licensee-Identified Violations

None.

2 Enclosure

REPORT DETAILS

Summary of Plant Status

Unit 2

With the exception of planned short duration reduction in power to support control rod pattern

adjustments, Unit 2 remained at or near full power for the entirety of the inspection period.

Unit 3

On January 28, operators reduced power to approximately 77 percent in an effort to control

rising exciter bearing no.11 trends, which was due to improperly tensioned turbine shaft

grounding brushes. Operators restored power to 100 percent on January 29, 2013.

On February 17, operators reduced power to approximately 96 percent for a planned insertion

of control rod drive G-8 for scram solenoid pilot valve repairs. Operators restored power to

100 percent on February 17, 2013.

With the exception of planned short duration reduction in power to support control rod pattern

adjustments, Unit 3 was maintained at or near full power for the remainder of the inspection

period.

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, and

Emergency Preparedness

1R01 Adverse Weather Protection (71111.01)

.1 Readiness for Impending Adverse Weather Condition - Extreme Cold Conditions

a. Inspection Scope

Since extreme cold conditions were forecast in the vicinity of the facility for

January 22, 2013, the inspectors reviewed the licensees overall preparations/protection

for the expected weather conditions. The inspectors walked down the cribhouse and the

125 volts-direct current (Vdc) and 250 Vdc battery systems because their safety related

functions could be affected or required as a result of the extreme cold conditions

forecast for the facility. The inspectors observed insulation, heat trace circuits, space

heater operation, and weatherized enclosures to ensure operability of affected systems.

The inspectors reviewed licensee procedures and discussed potential compensatory

measures with control room personnel. The inspectors focused on plant managements

actions for implementing the stations procedures for ensuring adequate personnel for

safe plant operation and emergency response would be available. Specific documents

reviewed during this inspection are listed in the Attachment to this report.

This inspection constituted one readiness for impending adverse weather condition

sample as defined in Inspection Procedure (IP) 71111.01-05.

3 Enclosure

b. Findings

No findings were identified.

.2 Readiness for Impending Adverse Weather Condition - High Wind Conditions

a. Inspection Scope

Since a strong winter storm with the potential for high winds was forecast in the vicinity

of the facility for January 29, 2013, the inspectors reviewed the licensees overall

preparations/protection for the expected weather conditions. The inspectors walked

down the high pressure coolant injection and isolation condenser systems, in addition to

the licensees emergency alternating current (AC) power systems, because their safety

related functions could be required as a result of high-winds-generated missiles or the

loss of offsite power. The inspectors evaluated the licensee staffs preparations against

the sites procedures and determined that the staffs actions were adequate. During the

inspection, the inspectors focused on plant-specific design features and the licensees

procedures used to respond to specified adverse weather conditions. The inspectors

also toured the plant grounds to look for any loose debris that could become missiles

from strong wind gusts. The inspectors evaluated operator staffing and accessibility of

controls and indications for those systems required to control the plant. Additionally, the

inspectors reviewed the Updated Final Safety Analysis Report (UFSAR) and

performance requirements for systems selected for inspection, and verified that operator

actions were appropriate as specified by plant specific procedures. The inspectors also

reviewed a sample of corrective action program (CAP) items to verify that the licensee

identified adverse weather issues at an appropriate threshold and dispositioned them

through the CAP in accordance with station corrective action procedures. Specific

documents reviewed during this inspection are listed in the Attachment to this report.

This inspection constituted one readiness for impending adverse weather condition

sample as defined in IP 71111.01-05.

b. Findings

No findings were identified.

.3 (Closed) Unresolved Item 05000237/2011003-01; 05000249/2011003-01, Failure to

Include Adequate Acceptance Criteria in a Surveillance Test

a. Inspection Scope

The inspectors reviewed the unresolved item and reviewed the resolution of Unresolved

Item (URI)05000237/2011004-01; 05000249/2011004-01, Classification of Emergency

Diesel-Driven Flood Pump to Required Quality Standards, in Section 4OA5.1 of this

report to determine whether a violation of any regulatory requirements existed.

b. Findings

Introduction: The inspectors identified a Finding having very low safety significance

(Green) for the failure to include adequate acceptance criteria in a surveillance test for

equipment that is the sole source of make-up water to the isolation condenser and spent

4 Enclosure

fuel pool for both units during a probable maximum flood (PMF) scenario as postulated

in the UFSAR.

Description: On April 8, 2011, the inspectors observed the performance of Work Order

(WO) 872864, D2/3 6Y PM Emergency Diesel Pump (Flood Pump) Operation. After

the surveillance was completed, the inspectors reviewed the completed work package

and identified that the work instructions did not include acceptance criteria for the

surveillance.

Work Order 872864 instructed the licensee, in part, to:

  • Throttle 2-inch brass valve until a discharge pressure of 50 psig (-0%, +2%) was

reached;

  • Record pump discharge pressure;
  • Record engine speed;
  • Record the number of gallons in the tank;
  • Record the time required to fill the tank.

Revision 2 of the WO instructions stated: Clarified work step no.19 to perform test or

tests at the discretion of the test engineer. Test discharge pressure to be determined by

test engineer. The test engineer determined that the 2-inch brass valve was to be

throttled until discharge pressures of 50, 75 and 100 pounds-force per square inch

gauge (psig) were reached.

Calculation DRE99-0035, Capacity and Discharge Head for Portable Isolation

Condenser Make-Up Pumps to be used during Flood Conditions, Revision 4,

determined that the most demanding hydraulic requirement for the flood pump is

350 gallons per minute (gpm) at 47 psig.

Dresden USFAR, Section 3.4.1.1, External Flood Protection Measures, states, in part,

that in the highly unlikely event that a PMF is predicted (528 feet (ft)) above mean sea

level (MSL)), the plant will shutdown in advance of the time predicted for flood stage

occurrence, i.e., grade level (517.5 ft). When the water level reaches 509 ft all reactors

will be shut down, the drywells will be deinerted, and the vessels will be flooded.

If the water level reaches 513 ft MSL at the plant site, cooling of the reactors will be

transferred to the isolation condensers, which will thereafter maintain the primary

system in a safe shutdown condition.

If forecast flood levels exceed 517 ft MSL, a diesel-driven emergency flood pump will be

connected by hoses to a fire system header in each unit. Through these fire system

headers, the emergency flood pump will be capable of providing at least 175 gpm of flow

to each unit. This flow will be used for make-up to the shell of the isolation condensers

and the spent fuel pools.

None of these requirements were referenced in the work order. Task 1 of WO 872864,

MM D2/3 6Y PM Emergency Diesel Pump (Flood Pump) Operation, stated that the

surveillance was found and left within acceptance criteria. The comments section of

Task 2 of WO 872864, Ops Support Flood Emergency Makeup Pump Maintenance,

stated there is no specific Acceptance Criteria in task-01.

5 Enclosure

As described in the Exelon Quality Assurance Manual, the licensee is committed to

follow the requirements of American National Standard Administrative Control and

Quality Assurance for the Operational Phase of Nuclear Power Plants

(ANSI/AN 3.2-1988). This standard states, in part, under Section 5.3.14, Test and

Inspection Procedures, that tests, including surveillance tests, and inspection

procedures contain or reference, as appropriate, acceptance criteria or limits contained

in applicable design or other source documents, such as vendors literature, engineering

drawings or plant specification that will be used to evaluate the results.

Similar issues were identified previously by the inspectors, involving surveillance

tests and operating procedures for the flood pump. Refer to non-cited violation

(NCV)05000237/2004010-02; 05000249/2004010-02, Source of Make-up Water,

URI 05000237/2006010-04; 05000249/2006010-04, Full Flow Testing of the Diesel

Driven Flood Pump at Design Conditions, and NCV 05000237/2007003-

04;05000249/2007003-04, Failure to Identify and Correct Issues with the Operation

and Testing of the Diesel Driven Pump Used to Respond to External Flooding.

Analysis: The inspectors determined that the failure to include acceptance criteria in a

surveillance test for equipment that is the sole source of make-up water to the isolation

condenser for both units during a PMF scenario did not meet ANSI/ANS 3.2-1988, a

performance deficiency warranting a significance evaluation in accordance with

Inspection Manual Chapter (IMC) 0612, Power Reactors Inspection Reports,

Appendix B, Issue Screening, issued on September 7, 2012. The inspectors

determined that the finding was more than minor because if left uncorrected, it could

lead to a more significant safety concern. Specifically, without any acceptance criteria in

the surveillance test, the licensee cannot determine whether the flood pump was able to

perform its function as described in the UFSAR and calculation DRE 99-0035.

The inspectors completed a Phase 1 significance determination of this finding using

IMC 0609, Significance Determination Process, Attachment 609.04, issued on

June 19, 2012. The inspectors determined that the finding impacted the Mitigating

Systems Cornerstone. The inspectors concluded that the diesel-driven make-up pump

would be a mitigating system in the case of the probable maximum flood. The

inspectors answered No to the questions on Exhibit 2 - Mitigating Systems Screening

Questions of Appendix A, The Significance Determination Process (SDP) For Findings

At-Power, of IMC 0609. As a result, the issue screened as of very low safety

significance (Green).

The inspectors determined that this finding has a cross-cutting aspect in the area of

Problem Identification and Resolution, Corrective Action Program, since it involves the

failure to ensure that issues potentially impacting nuclear safety are promptly identified,

fully evaluated, and that actions are taken to address safety issues in a timely manner,

commensurate with their significance. Specifically, the licensee failed to take

appropriate corrective actions to include acceptance criteria in a surveillance test for

equipment that is the sole source of make-up water to the isolation condenser and spent

fuel pool for both units during a PMF scenario as postulated in the UFSAR. As

discussed in the description section, similar issues were identified previously by the

inspectors, involving surveillance test and operating procedures for the flood pump.

P.1(d)

6 Enclosure

Enforcement: This finding does not involve enforcement action because, while a

performance deficiency existed, no violation of a regulatory requirement was identified.

The licensee generated issue reports (IR) 1209642, NRC Identified URI with Flood

Pump Acceptance Criteria, and 1487554, Follow-Up to IR to NRC Question on Diesel

Driven Flood Pump, to document the inspectors concerns. Corrective action includes

the development of acceptance criteria which ensure the pump meets licensing basis

requirements for a PMF event.

Because this finding does not involve a violation and is of very low safety or security

significance, it is identified as a FIN. (05000237/2013002-01; 05000249/2013002-01,

Failure to Include Acceptance Criteria in a Surveillance Test)

This URI is closed. This activity does not represent a completed inspection sample.

1R04 Equipment Alignment (71111.04Q and S)

.1 Quarterly Partial System Walkdowns

a. Inspection Scope

The inspectors performed partial system walkdowns of the following risk-significant

systems:

relay repair;

(HPCI) maintenance outage; and

  • Unit 3 IC during Unit 3 HPCI maintenance outage.

The inspectors selected these systems based on their risk significance relative to the

Reactor Safety Cornerstones at the time they were inspected. The inspectors attempted

to identify any discrepancies that could impact the function of the system and, therefore,

potentially increase risk. The inspectors reviewed applicable operating procedures,

system diagrams, UFSAR, TS requirements, outstanding work orders (WOs), condition

reports, and the impact of ongoing work activities on redundant trains of equipment in

order to identify conditions that could have rendered the systems incapable of

performing their intended functions. The inspectors also walked down accessible

portions of the systems to verify system components and support equipment were

aligned correctly and operable. The inspectors examined the material condition of the

components and observed operating parameters of equipment to verify that there were

no obvious deficiencies. The inspectors also verified that the licensee had properly

identified and resolved equipment alignment problems that could cause initiating events

or impact the capability of mitigating systems or barriers and entered them into the CAP

with the appropriate significance characterization. Documents reviewed are listed in the

Attachment to this report.

These activities constituted four partial system walkdown samples as defined in

IP 71111.04-05.

7 Enclosure

b. Findings

No findings were identified.

.2 Semi Annual Complete System Walkdown

a. Inspection Scope

On March 12, 2013, the inspectors performed a complete system alignment inspection

of the Unit 2 HPCI system to verify the functional capability of the system. This system

was selected because it was considered both safety significant and risk significant in the

licensees probabilistic risk assessment. The inspectors walked down the system to

review mechanical and electrical equipment lineups; electrical power availability; system

pressure and temperature indications, as appropriate; component labeling; component

lubrication; component and equipment cooling; hangers and supports; operability of

support systems; and to ensure that ancillary equipment or debris did not interfere with

equipment operation. A review of a sample of past and outstanding WOs was

performed to determine whether any deficiencies significantly affected the system

function. In addition, the inspectors reviewed the CAP database to ensure that system

equipment alignment problems were being identified and appropriately resolved.

Documents reviewed are listed in the Attachment to this report.

These activities constituted one complete system walkdown sample as defined in

IP 71111.04-05.

b. Findings

No findings were identified.

1R05 Fire Protection (71111.05)

.1 Routine Resident Inspector Tours (71111.05Q)

a. Inspection Scope

The inspectors conducted fire protection walkdowns which were focused on availability,

accessibility, and the condition of firefighting equipment in the following risk-significant

plant areas:

  • Fire Zone 8.2.5C, Unit 2 Lube Oil Room and Unit 2/3 Electro-hydraulic Control

Reservoir Area, Elevation 517;

  • Fire Zone 11.2.1, Unit 2 Southwest Corner Room, Elevation 476;
  • Fire Zone 11.2.3, Unit 2 HPCI Pump Room, Elevation 476; and
  • Fire Zone 9.0C, Unit 2/3 Swing Diesel Generator Room, Elevation 517.

The inspectors reviewed areas to assess if the licensee had implemented a fire

protection program that adequately controlled combustibles and ignition sources within

the plant, effectively maintained fire detection and suppression capability, maintained

passive fire protection features in good material condition, and implemented adequate

compensatory measures for out-of-service, degraded or inoperable fire protection

equipment, systems, or features in accordance with the licensees fire plan. The

inspectors selected fire areas based on their overall contribution to internal fire risk as

8 Enclosure

documented in the plants Individual Plant Examination of External Events with later

additional insights, their potential to impact equipment which could initiate or mitigate a

plant transient, or their impact on the plants ability to respond to a security event. Using

the documents listed in the Attachment to this report, the inspectors verified that fire

hoses and extinguishers were in their designated locations and available for immediate

use; that fire detectors and sprinklers were unobstructed; that transient material loading

was within the analyzed limits; and fire doors, dampers, and penetration seals appeared

to be in satisfactory condition. The inspectors also verified that minor issues identified

during the inspection were entered into the licensees CAP. Documents reviewed are

listed in the Attachment to this report.

These activities constituted four quarterly fire protection inspection samples as defined in

IP 71111.05-05.

b. Findings

No findings were identified.

1R06 Flooding (71111.06)

.1 Internal Flooding

a. Inspection Scope

The inspectors reviewed selected risk important plant design features and licensee

procedures intended to protect the plant and its safety-related equipment from internal

flooding events. The inspectors reviewed flood analyses and design documents,

including the UFSAR, engineering calculations, and abnormal operating procedures to

identify licensee commitments. The specific documents reviewed are listed in the

Attachment to this report. In addition, the inspectors reviewed licensee drawings to

identify areas and equipment that may be affected by internal flooding caused by the

failure or misalignment of nearby sources of water, such as the fire suppression or the

circulating water systems. The inspectors also reviewed the licensees corrective action

documents with respect to past flood related items identified in the corrective action

program to verify the adequacy of the corrective actions. The inspectors performed a

walkdown of the following plant area to assess the adequacy of watertight doors and

verify drains and sumps were clear of debris and were operable, and that the licensee

complied with its commitments:

  • Unit 3 containment cooling service water (CCSW) pump vault with a focus on the

floor drain system check valve.

Specific documents reviewed during this inspection are listed in the Attachment to this

report. This inspection constituted one internal flooding sample as defined in

IP 71111.06-05.

b. Findings

No findings were identified.

9 Enclosure

1R11 Licensed Operator Requalification Program (71111.11)

.1 Resident Inspector Quarterly Review of Licensed Operator Requalification (71111.11Q)

a. Inspection Scope

On February 8, 2013, the inspectors observed a crew of licensed operators in the plants

simulator during licensed operator requalification training to verify that operator

performance was adequate, evaluators were identifying and documenting crew

performance problems and training was being conducted in accordance with licensee

procedures. The inspectors evaluated the following areas:

  • licensed operator performance;
  • crews clarity and formality of communications;
  • ability to take timely actions in the conservative direction;
  • prioritization, interpretation, and verification of annunciator alarms;
  • correct use and implementation of abnormal and emergency procedures;
  • control board manipulations;
  • oversight and direction from supervisors; and
  • ability to identify and implement appropriate TS actions and Emergency Plan

actions and notifications.

The crews performance in these areas was compared to pre-established operator action

expectations and successful critical task completion requirements. Documents reviewed

are listed in the Attachment to this report.

This inspection constituted one quarterly licensed operator requalification program

simulator sample as defined in IP 71111.11.

b. Findings

No findings were identified.

.2 Resident Inspector Quarterly Observation of Heightened Activity or Risk (71111.11Q)

a. Inspection Scope

On January 29, 2013, the inspectors observed power ascension to 100 percent rated

thermal power (RTP) on Unit 3 and adverse condition monitoring of the main turbine

bearing no. 11 which had previously exhibited high temperatures and erratic vibrations.

The licensee previously lowered generator power output until temperature and vibrations

stabilized. The licensee determined the bearing was being adversely affected by static

voltages developing between the main turbine and the bearing metal which were the

resultant of the main turbine shaft ground brushes not being properly fastened to the

shaft at the conclusion of the previous refueling outage, D3R22, in December 2012.

Once the licensee restored adequate brush tension on the shaft the stray voltages were

alleviated and bearing conditions normalized. Prior to restoring plant conditions to full

power, the licensee consulted with the vendor to ensure bearing no. 11 was capable of

operating at rated conditions. This was an activity that required heightened awareness

or was related to increased risk. The inspectors evaluated the following areas:

10 Enclosure

  • licensed operator performance;
  • crews clarity and formality of communications;
  • ability to take timely actions in the conservative direction;
  • prioritization, interpretation, and verification of annunciator alarms (if applicable);
  • correct use and implementation of procedures;
  • control board (or equipment) manipulations;
  • oversight and direction from supervisors; and
  • ability to identify and implement appropriate TS actions and Emergency Plan

actions and notifications (if applicable).

The performance in these areas was compared to pre established operator action

expectations, procedural compliance and task completion requirements. Documents

reviewed are listed in the Attachment to this report.

This inspection constituted one quarterly licensed operator heightened activity/risk

sample as defined in IP 71111.11.

b. Findings

No findings were identified.

1R12 Maintenance Effectiveness (71111.12)

.1 Routine Quarterly Evaluations (71111.12Q)

a. Inspection Scope

The inspectors evaluated degraded performance issues involving the following

risk-significant system and evaluated the periodic assessment of the maintenance rule:

Assessment Period 10/1/2010 - 9/30/2012; and

  • 4 kv switchgear and circuit breakers.

The inspectors reviewed events such as where ineffective equipment maintenance had

or could have resulted in valid or invalid automatic actuations of engineered safeguards

systems and independently verified the licensee's actions to address system

performance or condition problems in terms of the following:

  • implementing appropriate work practices;
  • identifying and addressing common cause failures;
  • scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule;
  • characterizing system reliability issues for performance;
  • charging unavailability for performance;
  • trending key parameters for condition monitoring;
  • verifying appropriate performance criteria for structures, systems, and

components (SSCs)/functions classified as (a)(2), or appropriate and adequate

goals and corrective actions for systems classified as (a)(1).

11 Enclosure

The inspectors assessed performance issues with respect to the reliability, availability,

and condition monitoring of the system. In addition, the inspectors verified maintenance

effectiveness issues were entered into the CAP with the appropriate significance

characterization. Documents reviewed are listed in the Attachment to this report.

This inspection constituted two quarterly maintenance effectiveness samples as defined

in IP 71111.12-05.

b. Findings

No findings were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

.1 Maintenance Risk Assessments and Emergent Work Control

a. Inspection Scope

The inspectors reviewed the licensee's evaluation and management of plant risk for the

maintenance and emergent work activities affecting risk-significant and safety-related

equipment listed below to verify that the appropriate risk assessments were performed

prior to removing equipment for work:

  • Unit 2 Yellow Risk during the performance of DIS 1500-05 (24 month low

pressure coolant injection (LPCI) initiation circuitry testing);

  • Unit 2 Yellow Risk during 2B SBLC train inoperable for relay repair;
  • Unit 2 Yellow Risk during Division I CCSW work window;
  • Unit 2 Yellow Risk for U2 HPCI maintenance outage; and
  • Unit 3 Yellow Risk for U3 HPCI maintenance outage.

These activities were selected based on their potential risk significance relative to the

Reactor Safety Cornerstones. As applicable for each activity, the inspectors verified that

risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate

and complete. When emergent work was performed, the inspectors verified that the

plant risk was promptly reassessed and managed. The inspectors reviewed the scope

of maintenance work, discussed the results of the assessment with the licensee's

probabilistic risk analyst or shift technical advisor, and verified plant conditions were

consistent with the risk assessment. The inspectors also reviewed TS requirements and

walked down portions of redundant safety systems, when applicable, to verify risk

analysis assumptions were valid and applicable requirements were met. Specific

documents reviewed during this inspection are listed in the Attachment to this report.

These maintenance risk assessments and emergent work control activities constituted

five samples as defined in IP 71111.13-05.

b. Findings

No findings were identified.

12 Enclosure

1R15 Operability Determinations and Functional Assessments (71111.15)

.1 Operability Evaluations

a. Inspection Scope

The inspectors reviewed the following issues:

  • IR 1453700, Key Calculation Review Identifies Issues in DRE 98-0030;
  • Engineering Change Evaluation 39168, Unit 3 Drywell Equipment Drains Sump

Cover Plate Bent, Revision 0;

  • IR 1487125, U2 Isolation Condenser Support Nut Engagement Deficiency; and

The inspectors selected these potential operability issues based on the risk significance

of the associated components and systems. The inspectors evaluated the technical

adequacy of the evaluations to ensure that TS operability was properly justified and the

subject component or system remained available such that no unrecognized increase in

risk occurred. The inspectors compared the operability and design criteria in the

appropriate sections of the TS and UFSAR to the licensees evaluations to determine

whether the components or systems were operable. Where compensatory measures

were required to maintain operability, the inspectors determined whether the measures

in place would function as intended and were properly controlled. The inspectors

determined, where appropriate, compliance with bounding limitations associated with the

evaluations. Additionally, the inspectors reviewed a sampling of corrective action

documents to verify that the licensee was identifying and correcting any deficiencies

associated with operability evaluations. Documents reviewed are listed in the

Attachment to this report.

This operability inspection constituted five samples as defined in IP 71111.15-05.

b. Findings

No findings were identified.

1R18 Plant Modifications (71111.18)

.1 Plant Modifications

a. Inspection Scope

The inspectors reviewed the following modification:

Isolation Valve Closure SCRAM Circuit Functional Test, DOS 0500-08

The inspectors reviewed the configuration changes and associated 10 CFR 50.59 safety

evaluation screening against the design basis, the UFSAR, and the TS, as applicable, to

verify that the modification did not affect the operability or availability of the affected

system. The inspectors, as applicable, observed ongoing and completed work activities

13 Enclosure

to ensure that the modifications were installed as directed and consistent with the design

control documents; the modifications operated as expected; post-modification testing

adequately demonstrated continued system operability, availability, and reliability; and

that operation of the modifications did not impact the operability of any interfacing

systems. As applicable, the inspectors verified that relevant procedure, design, and

licensing documents were properly updated. Lastly, the inspectors discussed the plant

modification with operations, engineering, and training personnel to ensure that the

individuals were aware of how the operation with the plant modification in place could

impact overall plant performance. Documents reviewed in the course of this inspection

are listed in the Attachment to this report.

This inspection constituted one temporary plant modification samples as defined in

IP 71111.18-05.

b. Findings

No findings were identified.

1R19 Post-Maintenance Testing (71111.19)

.1 Post-Maintenance Testing

a. Inspection Scope

The inspectors reviewed the following post-maintenance (PM) activities to verify that

procedures and test activities were adequate to ensure system operability and functional

capability:

  • WO 1418376, Dresden Unit 2 Two Year PM Standby Diesel Generator

Inspection;

  • WO 1605861, D2 Quarterly TS HPCI [high pressure coolant injection] Pump

Operability Test and IST [in-service testing] Surveillance;

In-Service Test (IST) Surveillance; and

These activities were selected based upon the structure, system, or component's ability

to impact risk. The inspectors evaluated these activities for the following (as applicable):

the effect of testing on the plant had been adequately addressed; testing was adequate

for the maintenance performed; acceptance criteria were clear and demonstrated

operational readiness; test instrumentation was appropriate; tests were performed as

written in accordance with properly reviewed and approved procedures; equipment was

returned to its operational status following testing (temporary modifications or jumpers

required for test performance were properly removed after test completion); and test

documentation was properly evaluated. The inspectors evaluated the activities against

TSs, the UFSAR, 10 CFR Part 50 requirements, licensee procedures, and various

NRC generic communications to ensure that the test results adequately ensured that the

equipment met the licensing basis and design requirements. In addition, the inspectors

reviewed corrective action documents associated with post-maintenance tests to

determine whether the licensee was identifying problems and entering them in the CAP

14 Enclosure

and that the problems were being corrected commensurate with their importance to

safety. Documents reviewed are listed in the Attachment to this report.

This inspection constituted five post-maintenance testing samples as defined in

IP 71111.19-05.

b. Findings

No findings were identified.

1R22 Surveillance Testing (71111.22)

.1 Surveillance Testing

a. Inspection Scope

The inspectors reviewed the test results for the following activities to determine whether

risk-significant systems and equipment were capable of performing their intended safety

function and to verify testing was conducted in accordance with applicable procedural

and TS requirements:

  • WO 01407992, Recirculation Pump Running Differential Pressure Switch

Calibration (routine);

  • Unit 3 drywell floor drain sump and drywell equipment drain sump (RCS);

Surveillance MO3-1301-4 (routine);

  • WO 01616773, D2/3 1M TSTR/COM Diesel Fire Pump Operability Surveillance

(routine); and

  • WO 01396238, D2 Recirculation Flow Dual Limiter 262-26B (routine).

The inspectors observed in-plant activities and reviewed procedures and associated

records to determine the following:

  • did preconditioning occur;
  • the effects of the testing were adequately addressed by control room personnel

or engineers prior to the commencement of the testing;

  • acceptance criteria were clearly stated, demonstrated operational readiness, and

consistent with the system design basis;

  • plant equipment calibration was correct, accurate, and properly documented;
  • as-left setpoints were within required ranges; and the calibration frequency was

in accordance with TSs, the UFSAR, procedures, and applicable commitments;

  • measuring and test equipment calibration was current;
  • test equipment was used within the required range and accuracy; applicable

prerequisites described in the test procedures were satisfied;

  • test frequencies met TS requirements to demonstrate operability and reliability;

tests were performed in accordance with the test procedures and other

applicable procedures; jumpers and lifted leads were controlled and restored

where used;

  • test data and results were accurate, complete, within limits, and valid;
  • test equipment was removed after testing;

15 Enclosure

  • where applicable for inservice testing activities, testing was performed in

accordance with the applicable version of Section XI, ASMEs code, and

reference values were consistent with the system design basis;

  • where applicable, test results not meeting acceptance criteria were addressed

with an adequate operability evaluation or the system or component was

declared inoperable;

  • where applicable, actual conditions encountering high resistance electrical

contacts were such that the intended safety function could still be accomplished;

  • prior procedure changes had not provided an opportunity to identify problems

encountered during the performance of the surveillance or calibration test;

  • equipment was returned to a position or status required to support the

performance of its safety functions; and

  • all problems identified during the testing were appropriately documented and

dispositioned in the CAP.

Documents reviewed are listed in the Attachment to this report.

This inspection constituted four routine surveillance testing samples, one in-service

testing sample, and one reactor coolant system leak detection sample as defined in

IP 71111.22, Sections -02 and -05.

b. Findings

No findings were identified.

1EP6 Drill Evaluation (71114.06)

.1 Emergency Preparedness Drill Observation

a. Inspection Scope

The inspectors evaluated the conduct of a routine licensee emergency drill on

February 7, 2013, to identify any weaknesses and deficiencies in classification,

notification, and protective action recommendation development activities. The

inspectors observed emergency response operations in the Technical Support Center

to determine whether the event classification, notifications, and protective action

recommendations were performed in accordance with procedures. The inspectors also

attended the licensee drill critique to compare any inspector observed weakness with

those identified by the licensee staff in order to evaluate the critique and to verify

whether the licensee staff was properly identifying weaknesses and entering them into

the corrective action program. As part of the inspection, the inspectors reviewed the drill

package and other documents listed in the Attachment to this report.

This emergency preparedness drill inspection constituted one sample as defined in

IP 71114.06-05.

b. Findings

No findings were identified.

16 Enclosure

2. RADIATION SAFETY

CORNERSTONE: OCCUPATIONAL RADIATION SAFETY

2RS1 Radiological Hazard Assessment and Exposure Controls (71124.01)

This inspection constituted a partial sample as defined in IP 71124.01-05.

.1 Radiological Hazard Assessment (02.02)

a. Inspection Scope

The inspectors conducted walkdowns of the facility, including radioactive waste

processing, storage, and handling areas to evaluate material conditions and performed

independent radiation measurements to verify conditions.

b. Findings

No findings were identified.

.2 Instructions to Workers (02.03)

a. Inspection Scope

The inspectors selected various containers holding non-exempt licensed radioactive

materials that may cause unplanned or inadvertent exposure of workers, and assessed

whether the containers were labeled and controlled in accordance with 10 CFR 20.1904,

Labeling Containers, or met the requirements of 10 CFR 20.1905(g), Exemptions To

Labeling Requirements.

For work activities that could suddenly and severely increase radiological conditions,

the inspectors assessed the licensees means to inform workers of changes that could

significantly impact their occupational dose.

b. Findings

No findings were identified.

.3 Contamination and Radioactive Material Control (02.04)

a. Inspection Scope

The inspectors reviewed the licensees criteria for the survey and release of potentially

contaminated material. The inspectors evaluated whether there was guidance on how to

respond to an alarm that indicates the presence of licensed radioactive material.

The inspectors reviewed the licensees procedures and records to verify that the

radiation detection instrumentation was used at its typical sensitivity level based on

appropriate counting parameters. The inspectors assessed whether or not the licensee

has established a de facto release limit by altering the instruments typical sensitivity

through such methods as raising the energy discriminator level or locating the instrument

in a high-radiation background area.

17 Enclosure

b. Findings

No findings were identified.

.4 Radiological Hazards Control and Work Coverage (02.05)

a. Inspection Scope

The inspectors evaluated ambient radiological conditions (e.g., radiation levels or

potential radiation levels) during tours of the facility. The inspectors assessed whether

the conditions were consistent with applicable posted surveys, radiation work permits,

and worker briefings.

The inspectors evaluated the adequacy of radiological controls, such as required

surveys, radiation protection job coverage (including audio and visual surveillance for

remote job coverage), and contamination controls. The inspectors evaluated the

licensees use of electronic personal dosimeters in high noise areas as high radiation

area monitoring devices.

The inspectors examined the licensees physical and programmatic controls for highly

activated or contaminated materials, (nonfuel) stored within spent fuel and other storage

pools. The inspectors assessed whether appropriate controls, (i.e., administrative and

physical controls) were in place to preclude inadvertent removal of these materials from

the pool.

The inspectors examined the posting and physical controls for selected high radiation

areas and very high radiation areas to verify conformance with the occupational

performance indicator.

b. Findings

No findings were identified.

.5 Risk-Significant High Radiation Area and Very High Radiation Area Controls (02.06)

a. Inspection Scope

The inspectors discussed with the radiation protection manager the controls and

procedures for high-risk high radiation areas and very high radiation areas. The

inspectors discussed methods employed by the licensee to provide stricter control of

very high radiation area access as specified in 10 CFR 20.1602, Control of Access to

Very High Radiation Areas, and Regulatory Guide 8.38, Control of Access to High and

Very High Radiation Areas of Nuclear Plants. The inspectors assessed whether any

changes to licensee procedures substantially reduce the effectiveness and level of

worker protection.

The inspectors discussed the controls in place for special areas that have the potential

to become very high radiation areas during certain plant operations with first-line health

physics supervisors (or equivalent positions having backshift health physics oversight

authority). The inspectors assessed whether these plant operations require

communication beforehand with the health physics group, so as to allow corresponding

18 Enclosure

timely actions to properly post, control, and monitor the radiation hazards including re-

access authorization.

b. Findings

No findings were identified.

.6 Radiation Worker Performance (02.07)

a. Inspection Scope

The inspectors observed radiation worker performance with respect to stated radiation

protection work requirements. The inspectors assessed whether workers were aware of

the radiological conditions in their workplace and the radiation work permit controls/limits

in place, and whether their performance reflected the level of radiological hazards

present.

b. Findings

No findings were identified.

2RS6 Radioactive Gaseous and Liquid Effluent Treatment (71124.06)

This inspection constituted one complete sample as defined in IP 71124.06-05.

.1 Inspection Planning and Program Reviews (02.01)

Event Report and Effluent Report Reviews

a. Inspection Scope

The inspectors reviewed the radiological effluent release reports issued since the last

inspection to determine if the reports were submitted as required by the Offsite Dose

Calculation Manual/TSs. The inspectors reviewed anomalous results, unexpected

trends, or abnormal releases identified by the licensee for further inspection to determine

if they were evaluated, were entered in the corrective action program, and were

adequately resolved.

The inspectors identified radioactive effluent monitor operability issues reported by the

licensee as provided in effluent release reports, to review these issues during the onsite

inspection, as warranted, given their relative significance and determine if the issues

were entered into the CAP and adequately resolved.

b. Findings

No findings were identified.

19 Enclosure

Offsite Dose Calculation Manual and Final Safety Analysis Report Review

a. Inspection Scope

The inspectors reviewed UFSAR descriptions of the radioactive effluent monitoring

systems, treatment systems, and effluent flow paths so they could be evaluated during

inspection walkdowns.

The inspectors reviewed changes to the Offsite Dose Calculation Manual made by the

licensee since the last inspection against the guidance in NUREG-1301, 1302 and 0133,

and Regulatory Guides 1.109, 1.21 and 4.1. When differences were identified, the

inspectors reviewed the technical basis or evaluations of the change during the onsite

inspection to determine whether they were technically justified and maintain effluent

releases as-low-as-is-reasonably-achievable (ALARA).

The inspectors reviewed licensee documentation to determine if the licensee has

identified any non-radioactive systems that have become contaminated as disclosed

either through an event report or the Offsite Dose Calculation Manual since the last

inspection. This review provided an intelligent sample list for the onsite inspection of any

10 CFR 50.59 evaluations and allowed a determination if any newly contaminated

systems have an unmonitored effluent discharge path to the environment, whether any

required Offsite Dose Calculation Manual revisions were made to incorporate these new

pathways and whether the associated effluents were reported in accordance with

Regulatory Guide 1.21.

b. Findings

No findings were identified.

Groundwater Protection Initiative Program

a. Inspection Scope

The inspectors reviewed reported groundwater monitoring results and changes to the

licensees written program for identifying and controlling contaminated spills/leaks to

groundwater.

b. Findings

No findings were identified.

Procedures, Special Reports, and Other Documents

a. Inspection Scope

The inspectors reviewed Licensee Event Reports, event reports and/or special reports

related to the effluent program issued since the previous inspection to identify any

additional focus areas for the inspection based on the scope/breadth of problems

described in these reports.

The inspectors reviewed Effluent Program implementing procedures, particularly those

associated with effluent sampling, effluent monitor set-point determinations, and dose

calculations.

20 Enclosure

The inspectors reviewed copies of licensee and third party (independent) evaluation

reports of the Effluent Monitoring Program since the last inspection to gather insights

into the licensees program and aid in selecting areas for inspection review (smart

sampling).

b. Findings

No findings were identified.

.2 Walkdowns and Observations (02.02)

a. Inspection Scope

The inspectors walked down selected components of the gaseous and liquid discharge

systems to evaluate whether equipment configuration and flow paths aligned with the

documents reviewed in Section 2RS6.1 02.01 above and to assess equipment material

condition. Special attention was made to identify potential unmonitored release points

(such as open roof vents in boiling water reactor turbine decks, temporary structures

butted against turbine, auxiliary or containment buildings), building alterations which

could impact airborne, or liquid effluent controls, and ventilation system leakage that

communicates directly with the environment.

For equipment or areas associated with the systems selected for review that were not

readily accessible due to radiological conditions, the inspectors reviewed the licensee's

material condition surveillance records, as applicable.

The inspectors walked down filtered ventilation systems to assess for conditions such as

degraded high-efficiency particulate air/charcoal banks, improper alignment, or system

installation issues that would impact the performance or the effluent monitoring capability

of the effluent system.

As available, the inspectors observed selected portions of the routine processing and

discharge of radioactive gaseous effluent (including sample collection and analysis) to

evaluate whether appropriate treatment equipment was used and the processing

activities align with discharge permits.

The inspectors determined if the licensee has made significant changes to their effluent

release points, (e.g., changes subject to a 10 CFR 50.59 review) or require NRC

approval of alternate discharge points.

As available, the inspectors observed selected portions of the routine processing and

discharge liquid waste (including sample collection and analysis) to determine if

appropriate effluent treatment equipment is being used and that radioactive liquid waste

is being processed and discharged in accordance with procedure requirements and

aligns with discharge permits.

b. Findings

No findings were identified.

21 Enclosure

.3 Sampling and Analyses (02.03)

a. Inspection Scope

The inspectors selected effluent sampling activities, consistent with smart sampling, and

assessed whether adequate controls have been implemented to ensure representative

samples were obtained (e.g., provisions for sample line flushing, vessel recirculation,

composite samplers, etc.)

The inspectors selected effluent discharges made with inoperable (declared out-of-

service) effluent radiation monitors to assess whether controls were in place to ensure

compensatory sampling was performed consistent with the radiological effluent

TSs/Offsite Dose Calculation Manual and that those controls were adequate to prevent

the release of unmonitored liquid and gaseous effluents.

The inspectors determined whether the facility was routinely relying on the use of

compensatory sampling in lieu of adequate system maintenance, based on the

frequency of compensatory sampling since the last inspection.

The inspectors reviewed the results of the Inter-Laboratory Comparison Program to

evaluate the quality of the radioactive effluent sample analyses and assessed whether

the Inter-Laboratory Comparison Program includes had-to-detect isotopes as

appropriate.

b. Findings

No findings were identified.

.4 Instrumentation and Equipment (02.04)

Effluent Flow Measuring Instruments

a. Inspection Scope

The inspectors reviewed the methodology the licensee uses to determine the effluent

stack and vent flow rates to determine if the flow rates were consistent with Radiological

Effluent Technical Specifications/Offsite Dose Calculation Manual or UFSAR values, and

that differences between assumed and actual stack and vent flow rates did not affect the

results of the projected public doses.

b. Findings

No findings were identified.

Air Cleaning Systems

a. Inspection Scope

The inspectors assessed whether surveillance test results since the previous inspection

for TSs required ventilation effluent discharge systems (high-efficiency particulate air

and charcoal filtration), such as the Standby Gas Treatment System and the

Containment/Auxiliary Building Ventilation System, met Technical Specifications

acceptance criteria.

22 Enclosure

b. Findings

No findings were identified.

.5 Dose Calculations (02.05)

a. Inspection Scope

The inspectors reviewed all significant changes in reported dose values compared to the

previous radiological effluent release report (e.g., a factor of 5, or increases that

approach Appendix I criteria) to evaluate the factors which may have resulted in the

change.

The inspectors reviewed radioactive liquid and gaseous waste discharge permits to

assess whether the projected doses to members of the public were accurate and based

on representative samples of the discharge path.

Inspectors evaluated the methods used to determine the isotopes that are included in

the source term to ensure all applicable radionuclides are included within detectability

standards. The review included the current Part 61 analyses to ensure hard-to-detect

radionuclides are included in the source term.

The inspectors reviewed changes in the licensees offsite dose calculations since the

last inspection to evaluate whether changes were consistent with the Offsite Dose

Calculation Manual and Regulatory Guide 1.109. Inspectors reviewed meteorological

dispersion and deposition factors used in the Offsite Dose Calculation Manual and

effluent dose calculations to evaluate whether appropriate factors were being used for

public dose calculations.

The inspectors reviewed the latest Land Use Census to assess whether changes (e.g.,

significant increases or decreases to population in the plant environs, changes in critical

exposure pathways, the location of nearest member of the public, or critical receptor, etc.)

have been factored into the dose calculations.

For the releases reviewed above, the inspectors evaluated whether the calculated doses

(monthly, quarterly, and annual dose) are within the 10 CFR Part 50, Appendix I and

TSs dose criteria.

The inspectors reviewed, as available, records of any abnormal gaseous or liquid tank

discharges (e.g., discharges resulting from misaligned valves, valve leak-by, etc) to

ensure the abnormal discharge was monitored by the discharge point effluent monitor.

Discharges made with inoperable effluent radiation monitors, or unmonitored leakages

were reviewed to ensure that an evaluation was made of the discharge to satisfy

10 CFR 20.1501 so as to account for the source term and projected doses to the public.

b. Findings

No findings were identified.

23 Enclosure

.6 Groundwater Protection Initiative Implementation (02.06)

a. Inspection Scope

The inspectors reviewed monitoring results of the Groundwater Protection Initiative to

determine if the licensee had implemented its program as intended and to identify any

anomalous results. For anomalous results or missed samples, the inspectors assessed

whether the licensee had identified and addressed deficiencies through its CAP.

The inspectors reviewed identified leakage or spill events and entries made into

10 CFR 50.75 (g) records. The inspectors reviewed evaluations of leaks or spills and

reviewed any remediation actions taken for effectiveness. The inspectors reviewed

onsite contamination events involving contamination of ground water and assessed

whether the source of the leak or spill was identified and mitigated.

For unmonitored spills, leaks, or unexpected liquid or gaseous discharges, the

inspectors assessed whether an evaluation was performed to determine the type

and amount of radioactive material that was discharged by:

Assessing whether sufficient radiological surveys were performed to evaluate the

extent of the contamination and the radiological source term and assessing

whether a survey/evaluation had been performed to include consideration of

hard-to-detect radionuclides.

Determining whether the licensee completed offsite notifications, as provided in

its Groundwater Protection Initiative implementing procedures.

The inspectors reviewed the evaluation of discharges from onsite surface water bodies

that contain or potentially contain radioactivity, and the potential for ground water

leakage from these onsite surface water bodies. The inspectors assessed whether the

licensee was properly accounting for discharges from these surface water bodies as part

of their effluent release reports.

The inspectors assessed whether on-site ground water sample results and a description

of any significant on-site leaks/spills into ground water for each calendar year were

documented in the Annual Radiological Environmental Operating Report for the

Radiological Environmental Monitoring Program or the Annual Radiological Effluent

Release Report for the Radiological Effluent TSs.

For significant, new effluent discharge points (such as significant or continuing leakage

to ground water that continues to impact the environment if not remediated), the

inspectors evaluated whether the offsite dose calculation manual was updated to include

the new release point.

b. Findings

No findings were identified.

24 Enclosure

.7 Problem Identification and Resolution (02.07)

a. Inspection Scope

Inspectors assessed whether problems associated with the Effluent Monitoring and

Control Program were being identified by the licensee at an appropriate threshold and

were properly addressed for resolution in the licensee CAP. In addition, they evaluated

the appropriateness of the Corrective Actions for a selected sample of problems

documented by the licensee involving radiation monitoring and exposure controls.

b. Findings

No findings were identified.

4. OTHER ACTIVITIES

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency

Preparedness, Occupational Radiation Safety, Public Radiation Safety, and

Security

4OA1 Performance Indicator Verification (71151)

.1 Unplanned Scrams per 7000 Critical Hours

a. Inspection Scope

The inspectors sampled licensee submittals for the Unplanned Scrams per 7000 Critical

Hours (IE01) performance indicator (PI) for Dresden Nuclear Power Station Units 2

and 3 covering the period from the first through fourth quarter 2012. To determine the

accuracy of the PI data reported during those periods, PI definitions and guidance

contained in the Nuclear Energy Institute (NEI) Document 99-02, Regulatory

Assessment Performance Indicator Guideline, Revision 6, dated October 2009, were

used. The inspectors reviewed the licensees operator narrative logs, issue reports,

event reports and NRC Integrated Inspection Reports for the period of first through the

fourth quarter 2012 to validate the accuracy of the submittals. The inspectors also

reviewed the licensees issue report database to determine if any problems had been

identified with the PI data collected or transmitted for this indicator and none were

identified. Documents reviewed are listed in the Attachment to this report.

This inspection constituted two unplanned scrams per 7000 critical hours samples as

defined in IP 71151-05.

b. Findings

No findings were identified.

.2 Unplanned Scrams with Complications

a. Inspection Scope

The inspectors sampled licensee submittals for the Unplanned Scrams with

Complications (IE02) performance indicator for Dresden Nuclear Power Station Units 2

and 3 covering the period from the first through the fourth quarter 2012. To determine

25 Enclosure

the accuracy of the PI data reported during those periods, PI definitions and guidance

contained in the NEI Document 99-02, Regulatory Assessment Performance Indicator

Guideline, Revision 6, dated October 2009, were used. The inspectors reviewed the

licensees operator narrative logs, issue reports, event reports and NRC Integrated

Inspection Reports for the period of first through the fourth quarter 2012 to validate the

accuracy of the submittals. The inspectors also reviewed the licensees issue report

database to determine if any problems had been identified with the PI data collected or

transmitted for this indicator and none were identified. Documents reviewed are listed in

the Attachment to this report.

This inspection constituted two unplanned scrams with complications samples as

defined in IP 71151-05.

b. Findings

No findings were identified.

.3 Unplanned Transients per 7000 Critical Hours

a. Inspection Scope

The inspectors sampled licensee submittals for the Unplanned Transients per 7000

Critical Hours (IE03) performance indicator Dresden Nuclear Power Station Units 2

and 3 covering the period from the first through the fourth quarter 2012. To determine

the accuracy of the PI data reported during those periods, PI definitions and guidance

contained in the NEI Document 99-02, Regulatory Assessment Performance Indicator

Guideline, Revision 6, dated October 2009, were used. The inspectors reviewed the

licensees operator narrative logs, issue reports, maintenance rule records, event

reports, and NRC Integrated Inspection Reports for the period of first through the fourth

quarter 2012 to validate the accuracy of the submittals. The inspectors also reviewed

the licensees issue report database to determine if any problems had been identified

with the PI data collected or transmitted for this indicator and none were identified.

Documents reviewed are listed in the Attachment to this report.

This inspection constituted two unplanned transients per 7000 critical hours samples as

defined in IP 71151-05.

b. Findings

No findings were identified.

4OA2 Identification and Resolution of Problems (71152)

.1 Routine Review of Items Entered into the Corrective Action Program

a. Inspection Scope

As part of the various baseline inspection procedures discussed in previous sections of

this report, the inspectors routinely reviewed issues during baseline inspection activities

and plant status reviews to verify they were being entered into the licensees CAP at an

appropriate threshold, that adequate attention was being given to timely corrective

actions, and that adverse trends were identified and addressed. Attributes reviewed

26 Enclosure

included: identification of the problem was complete and accurate; timeliness was

commensurate with the safety significance; evaluation and disposition of performance

issues, generic implications, common causes, contributing factors, root causes,

extent-of-condition reviews, and previous occurrences reviews were proper and

adequate; and that the classification, prioritization, focus, and timeliness of corrective

actions were commensurate with safety and sufficient to prevent recurrence of the issue.

Minor issues entered into the licensees CAP as a result of the inspectors observations

are included in the Attachment to this report.

These routine reviews for the identification and resolution of problems did not constitute

any additional inspection samples. Instead, by procedure they were considered an

integral part of the inspections performed during the quarter and documented in

Section 1 of this report.

b. Findings

No findings were identified.

.2 Daily Corrective Action Program Reviews

a. Inspection Scope

In order to assist with the identification of repetitive equipment failures and specific

human performance issues for follow-up, the inspectors performed a daily screening of

items entered into the licensees CAP. This review was accomplished through

inspection of the stations daily condition report packages.

These daily reviews were performed by procedure as part of the inspectors daily plant

status monitoring activities and, as such, did not constitute any separate inspection

samples.

b. Findings

No findings were identified.

.3 Selected Issue Follow-Up Inspection: Review of the Sites Procedural and Physical

Modifications for the Response to a Probable Maximum Flood Event

a. Inspection Scope

In August 2012, as required by a letter from the NRC to licensees entitled, Request for

Information Pursuant to Title 10 of the Code of Federal Regulations 50.54(f) Regarding

Recommendations 2.1, 2.3, and 9.3, of the Near-Term Task Force Review of Insights

from the Fukushima Dai-Ichi Accident, dated March 12, 2012 (ADAMS Accession

No. ML12053A340), the licensee performed external flooding vulnerability walk downs of

the site and a reasonable simulation of the flood response Abnormal Operating

Procedure DOA 0010-04, Floods, under the observation of the sites NRC resident

inspectors and NRC staff from the Japan Lessons Learned Directorate (JLD). The

results of the simulation and walk downs indicated that the licensee could perform the

procedure as written, except potentially for several non-critical steps, within the

appropriate timeline and that the procedure could achieve its goal of placing both Units 2

and 3 in a Hot Shutdown condition (Mode 3) and maintaining each units respective

27 Enclosure

spent fuel pool filled with make-up water. Many areas for improvement with the

procedure were identified, but no specific issue was identified that by itself could be

shown as preventing the licensee from achieving the desired end state within the time

line identified by the 1982, Hydrological Considerations Technical Evaluation Report

which defines the PMF scenario at the Dresden Nuclear Power Station. The PMF for

Dresden assumes a severe precipitation event covering northern Illinois and Indiana

which results in flood still water levels reaching 525 ft above mean sea level (MSL) with

wave run up reaching 528 ft MSL. Ground elevation at Dresden is 517.5 ft MSL with

Illinois River level maintained at approximately 505 ft MSL by the downstream U. S.

Army Corps of Engineers controlled Dresden Island Lock and Dam.

The sites flooding response requires opening safety related structures including the

reactor building to the environment once flood levels reach site grade (517.5 ft MSL)

allowing flood waters to enter, as the structures are not designed to resist the static force

of the flood water on their outer walls. This results in a station blackout as offsite and

onsite AC electrical power would be unavailable and emergency core cooling systems

(ECCS) and other sources of cooling and injection would not be available as they are

submerged by the flood waters or are without electrical power to operate. To cope with

this condition, the licensee would operate a diesel-powered pump which will be

connected to the fire protection system and provide water from the flooded reactor

building to the shell side of each units isolation condenser to remove decay heat from

the reactors and provide make-up water to both spent fuel pools. The flood pump was

originally to be supported above the flood waters by a chain fall mounted to a jib crane in

the reactor building track way, but can now be mounted on a floating dock which would

be staged in the reactor building trackway in the lead up to the flood waters reaching site

grade.

The inspectors performed a historical review of DOA 0010-04, Floods, from its origin

until the current revision (Revision 38); observed the licensees performance during

numerous simulations and actual demonstrations of portions of the flood strategy;

ensured the availability of various instruments, gauges and indications relied upon by the

licensee to implement the flood strategy; reviewed the licensees implementation plans

for the Aqua-Dam; assisted Headquarters and Regional management in developing and

reviewing follow-up questions for the licensee; and reviewed the licensees future plans

for structurally modifying the reactor building in order to ensure adequate strength to

resist the static forces of the flood waters and to ensure its water-tight integrity. This

structural modification is intended to maintain the reactor building free from flooding and

as such ensure the availability of onsite emergency AC power and numerous safety

related systems installed in the plant to keep the reactors safely shut down.

This review constituted one in-depth problem identification and resolution sample as

defined in IP 71152-05.

b. Findings and Observations

Following the walk downs and simulation, the licensee along with a contracted

engineering firm who observed these activities, developed a number of mitigating

strategies for external flood events impacting the site up to and including the PMF. As

previously noted, the site becomes vulnerable to flooding as soon as flood waters reach

site grade. As a result, the licensee has purchased equipment and revised procedures

to mitigate the impact on the site from an external flood. In addition, the NRC has raised

28 Enclosure

a number of questions and concerns regarding the outcome of the walk downs and

reasonable simulation. These questions were submitted in a 30 day response letter to

the licensee on November 1, 2012, (ML12306A393) with the licensee response to these

questions received on December 1, 2012 (ML12348A012). The initial round of NRC

questions along with licensee identified weaknesses in the sites response strategy

resulted in the following enhancements and mitigating strategies being developed:

1) Enhancements

  • Attachments were added to DOA 0010-04 which specifically list electrical buses

to be de-energized and underground fuel tanks to be filled prior to flood waters

reaching site grade.

  • The purchase of four motor boats maintained in the owner controlled area (OCA)

for use of moving personnel around the site instead of having to rely on offsite

assets.

  • The addition of the floating dock to mount the diesel-driven flood pump and six

diesel fuel barrels provides a more stable platform that will naturally adjust to

changing flood height levels as compared to suspending the pump from a chain

fall strung from the reactor building jib crane.

  • Purchasing back up floating gas powered drafting pumps which can be used in

the event the diesel-driven flood pump needs to be taken out of service.

  • Flood height markers added in the reactor building trackway and the cribhouse

will assist the site in trending flood waters.

  • Licensee follow up to the reasonable simulation identified that during the early

stages of the flooding event, when level in the reactor building was still relatively

shallow, it is possible for air in addition to water to be drawn into the suction of

the flood pump. The licensee enhanced the flood procedure to direct operators

to put the flood pump suction line into the CRD pull-put channel to increase its

submergence and minimize the possibility of air binding the pump.

2) Mitigating Strategies

  • The acquisition of 4000 feet of Aqua-Dam to provide protection for the power

block for floods up to 5.5 feet above ground elevation. The berm is stored on two

53 foot long flatbeds parked in the OCA for deployment. The licensee also had a

custom bridge/dock made to be able to transport personnel over the Aqua-Dam

to boats/land on either side.

  • Installation of flood barriers at the isolation condenser make-up pump house to

reduce the amount of time and personnel required to provide flood protection to

this structure early in the event. At the time of the reasonable simulation, the

licensee provided two feet of flood protection by building a sand bag berm which

required approximately 8.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> to construct. The addition of the barriers

provides four feet of flood mitigation and only requires maintenance technicians

two hours to deploy. Providing this protection allows the site to rely on plant

installed equipment to provide make up to the isolation condensers removing

reactor decay heat for lesser flooding events and delaying the transition to the

dock mounted diesel flood pump which would still be providing make-up to the

reactors and spent fuel pools.

  • The licensee developed Technical Support Guideline (TSG) - 3, Attachment T,

which created a proceduralized pathway to add make-up water to the reactors

utilizing the pressurized fire header, through test connections in the SBLC,

29 Enclosure

directly to the reactor for both units if make-up via a traditional means is not able

to be restored. The licensee also modified the flooding procedure to instruct

operators to close the reactor recirculation loop isolation valves isolating

recirculation pump seals from the reactor and removing a potential source of

reactor coolant inventory loss.

The NRC submitted a second round of questions to the licensee on January 3, 2013,

with a focus on several of the enhancements and mitigating strategies recently

implemented and follow-up on the licensees original responses (ML13003A226). The

licensee responded on January 31, 2013, to the NRCs inquiries (ML13037A045).

Through review of the licensees responses to the staffs concerns in addition to

observing the reasonable simulation, the inspectors noted that the licensees procedure

for monitoring canal level as the flood waters rose above 509 ft. MSL required the use of

canal level instrumentation. In particular, a level transmitter that could be read remotely

from the control room as Plant Process Computer point E354 was called out as the

primary means of determining flood level until flood waters reached site grade at 517.5 ft

MSL. The flood procedure also allowed operators to manually identify flood level in the

cribhouse with a tape measure or other level indicator if the canal level indicator was not

available. During the reasonable simulation and prior, the E354 computer point was not

functioning and Dresden operators would have always had to rely on local, manual

actions to identify flood levels between 509 ft MSL and 517.5 ft MSL. It should be noted

that following the NRCs Systematic Evaluation Program review of Unit 2 in 1982, the

licensee committed in a letter from Thomas J. Rausch to Paul OConnor titled,

Dresden 2 SEP Topic: II-3.B, Flooding Potential and Protective Requirements; II-3.B.1,

Capability of Operating Plants to Cope with Design Basis Flood Conditions; and II-3.C,

Safety Related Water Supply (Ultimate Heat Sink), dated November 17, 1982, to install

a level gauge in the intake canal. The inspectors noted that this level gauge was not

operational for several years or may have never been operational requiring the operators

to perform manual actions to identify flood height. In addition to performing several

actions directed by DOA 0010-04 based on the flood water height prior to reaching site

grade as measured by operators, the Dresden Emergency Plan requires the site to

declare an ALERT under Emergency Action Level (EAL) HA4 when intake canal level

reaches 513 ft MSL. The inspectors determined that not meeting a NRC commitment in

that an operational canal level indicator was not installed following the Systematic

Evaluation Program review of Unit 2 in 1982 was a performance deficiency. This

performance deficiency was not more than minor in that the licensee had procedurally

driven compensatory measures in place and possessed the equipment necessary to

accurately measure flood water height between 509 ft MSL and 517.5 ft MSL and as a

result would have been capable of performing the flooding response strategy and carry

out the sites Emergency Plan.

The inspectors identified a second performance deficiency associated with no licensee

procedure for providing make-up water to the reactor coolant system while flood waters

are above site grade level.

Introduction: A finding preliminarily determined to be of low to moderate safety

significance (White) and an associated Apparent Violation (AV) of TS Section 5.4.1 was

identified by the inspectors, in that, prior to November 2012, the licensees procedures

and specifically Abnormal Operating Procedure (AOP) DOA 0010-04, Floods, did not

account for reactor inventory make up during an external flooding scenario up to and

30 Enclosure

including the PMF event which could result in reactor vessel water level lowering below

top of active fuel (TAF) leading to core damage.

Description: In August 2012, the licensee performed a reasonable simulation of its

external flooding strategy for coping with a PMF event. The inspectors subsequently

noted that the flood strategy did not contain steps accounting for losses in reactor vessel

inventory. Under normal plant conditions there are both unidentified and identified

leakage paths from the reactor coolant system. During the PMF event, systems which

would provide normal and emergency make up capacity to the reactors would be

inundated by the flood waters and would not be available.

The NRC questioned the licensee regarding this concern in a 30 day response letter to

the licensee on November 1, 2012 (ML12306A393). In response to this concern, the

licensee developed TSG-3, Attachment T, effective November 21, 2012, proceduralizing

the use of the fire protection header which would be pressurized and supplied by the

diesel flood pump to supply through mechanical adapters, which are labeled and stored

above projected PMF flood levels, the reactor by connecting to test connections in the

SBLC system. The licensee also revised DOA 0010-04, Floods, directing operators to

shut reactor recirculation loop isolation valves to reduce potential reactor leakage

sources to those governed by the unidentified leakage Technical Specification.

The licensee determined that with reactor unidentified leakage at 5 gpm, the maximum

permitted by TS, it would take approximately 130 hours0.0015 days <br />0.0361 hours <br />2.149471e-4 weeks <br />4.9465e-5 months <br /> to reach a reactor water level at

the TAF. The Dresden PMF hydrograph indicates that flood waters would exist at site

grade for approximately 57 hours6.597222e-4 days <br />0.0158 hours <br />9.424603e-5 weeks <br />2.16885e-5 months <br />. After the flood waters recede, the licensee identified

that TSG-3 Attachment H, Reactor Pressure Vessel Injection Using Portable Diesel

Driven Pump, could be used to provide injection by tying a dedicated diesel driven

FLEX pump (three are maintained onsite) into the fire protection ring header and

injecting to each units reactor vessel through the low pressure coolant injection system.

In addition, after the flood waters recede, mechanical level instruments for the entire fuel

zone would once again be available to the operators.

The inspectors challenged the licensees leakage assertion in that TS permit a total

leakage rate of up to 25 gpm which would significantly reduce the amount of time until

TAF is reached under the worst case permitted leakage conditions in the reactor coolant

system. The inspectors based this concern on the fact that the licensee did not originally

employ the strategy for isolating reactor recirculation loops which would make them

susceptible to losses due to both unidentified and identified pathways. During the site

flood event operators would be limited in their ability to monitor reactor water level as the

mechanical level indicator called out by licensee procedures has an indication band

between +60 inches and - 60 inches of water. Top of active fuel for Dresden is

considered at -143 inches of water. As a result, operators would have to provide make

up to the reactor vessel much sooner than 130 hours0.0015 days <br />0.0361 hours <br />2.149471e-4 weeks <br />4.9465e-5 months <br /> in order for level in the reactor to

not become indeterminate or possibly reach TAF during the 57 hours6.597222e-4 days <br />0.0158 hours <br />9.424603e-5 weeks <br />2.16885e-5 months <br /> the flood waters

inundate the site.

The licensee reviewed its inventory of procedures prior to November 2012 up to and

including the Severe Accident Mitigation Guidelines and was not able to identify written

instructions for operators attempting to control reactor vessel level under station blackout

conditions with high pressure coolant injection and all installed diesel driven systems

31 Enclosure

(fire protection) unavailable to provide injection capacity, which would be the situation on

site while flood waters were present.

Analysis: The inspectors determined that the licensees failure to consider reactor

vessel inventory make up during an external flooding scenario up to and including the

PMF was a performance deficiency warranting a significance evaluation. The finding

was determined to be more than minor in accordance with Inspection Manual

Chapter (IMC) 0612, Power Reactor Inspection Reports, Appendix B, Issue

Screening, dated September 7, 2012, because it was associated with the Mitigating

Systems Cornerstone attribute of procedure quality and adversely affected the

cornerstone objective to ensure the availability, reliability, and capability of systems that

respond to initiating events to prevent undesirable consequences.

The inspectors determined the finding could be evaluated using the SDP in accordance

with IMC 0609, Significance Determination Process, Attachment 0609.04, Initial

Characterization of Findings, dated June 19, 2012, and Appendix A, The Significance

Determination Process (SDP) for Findings At-Power, Exhibit 2, Mitigating Systems

Screening Questions, dated June 19, 2012. The inspectors answered YES to the

External Event Mitigation question which directed them to Exhibit 4, External Events

Screening Questions. The inspectors determined the statement that the finding would

degrade one or more trains of a system that supports a risk significant system or

function was TRUE and as a result a detailed risk evaluation was required.

A Significance and Enforcement Review Panel (SERP) determined that IMC 0609,

Appendix M, Significance Determination Process Using Qualitative Criteria, dated

April 12, 2012, was appropriate to use due to the lack of existing quantitative SDP tools

for evaluating external flooding risk. As part of that process, the Region III Senior

Reactor Analyst (SRA) developed a simple event tree model to perform a bounding

quantitative evaluation. The model represents an external flood event that exceeds

grade level elevation (517.5) and requires implementation of the flood procedure,

DOA 0010-04, Floods, Revision 32.

The input assumptions were highly uncertain and were varied to calculate a range of risk

estimates. The values for flood frequency, the probability of reactor pressure vessel

leakage requiring makeup, and the likelihood of successful makeup to the vessel during

and after the flood recedes were key inputs to the evaluation. The change in core

damage frequency (CDF) estimates ranged from Green, a finding of very low safety

significance, to Yellow, a finding of substantial safety significance. For the quantitative

evaluation, the flood frequency was varied from 1E-4/yr to 1E-6/yr. The probability of

reactor pressure vessel leakage requiring inventory makeup was varied from 1.0,

makeup would always be required, to .02, makeup would be required 2 percent of the

time. To represent the change in risk due to the performance deficiency, the SRA

assumed that reactor pressure vessel (RPV) makeup during the flood would not be

successful and that makeup after the flood would have a failure probability ranging from

0.1 to 0.5. For the base case, absent the performance deficiency, the SRA assumed

that a makeup strategy would be available both during and after the flood and that the

nominal failure probability would be much lower than in the performance deficiency case.

For the evaluation of the qualitative decision-making attributes, the NRC determined that

defense-in-depth, safety margin, and the period of time the performance deficiency

existed were the most important factors.

32 Enclosure

The flood procedure did not provide for defense-in-depth for reactor inventory control

during a flood event. A flood greater than elevation 517.5 ft will fail sources of reactor

inventory makeup including feedwater, condensate, control rod drive injection, fire

pumps, service water and all ECCS. Recovery of plant systems after the flood is not

likely to be successful and the use of alternate temporary systems after the flood

recedes was not specified in the flood procedure. Plant shutdown under flooding

conditions would require the implementation of many diverse plant procedures which are

not well integrated into the flood procedure. The lack of integrated procedures combined

with the lack of flood level predictive capabilities could result in variable plant conditions

at the onset of significant flood impacts. As a result, the need for inventory makeup

during the flood is possible. Also, the defense-in-depth barriers of secondary

containment and primary containment are degraded during the implementation of the

flood procedure.

The licensee did not have an administrative limit for reactor operation with reactor vessel

leakage, only TS limits. The lack of a conservative limit allowed no safety margin

between operational practices and TS limits.

The performance deficiency represents a longstanding issue. In 1982 the PMF scenario

was initially identified. The licensee had the potential to identify that, during an extended

site inundation flooding event, there would be a need to have planned actions to

maintain RPV inventory but did not identify that need until the lack of a proceduralized

method was questioned by the NRC.

A SERP held on April 18, 2013, made a preliminary determination that the finding was of

low to moderate safety significance (White) based on the quantitative and qualitative

evaluations. Considerations involved in that determination included the minimal defense

in depth for addressing reactor vessel makeup, lack of administrative limits for reactor

vessel leakage, that during a flooding event the operators would be required to

implement numerous procedures which did not appear to be well integrated into the

flooding response procedure, that the licensee had numerous opportunities recently and

in the past to identify and then address the deficiency of not addressing a reactor

makeup method, and the length of time the performance deficiency existed.

The inspectors determined that this finding has a cross-cutting aspect in the area of

Problem Identification and Resolution, CAP, Self and Independent Assessments, since it

involves the failure to identify the lack of procedural steps to address a critical function

during a comprehensive self assessment of the flooding strategy. Specifically, the

licensee failed to conduct a self assessment with sufficient depth when reviewing the

sites flooding strategy during a reasonable simulation and comprehensive flooding

strategy site walk down in August 2012. (P.3(a))

Enforcement: Technical Specification 5.4.1 requires in part, that written procedures be

established, implemented, and maintained covering the following activities: the

applicable procedures recommended in Regulatory Guide (RG) 1.33. Revision 2,

Appendix A, February 1978. RG 1.33. Revision 2, Appendix A, Paragraph 6, addresses

Procedures for Combating Emergencies and Other Significant Events and Item w

addresses Acts of Nature (e.g ., tornado, flood, dam failure, earthquakes). An AV of

TS 5.4.1 has been identified in that, from February 20, 1991, to November 21, 2012, the

licensee failed to ensure procedures existed which ensured reactor vessel inventory

could be maintained during external floods. Specifically, DOA 0010-04, Floods, did not

33 Enclosure

account for reactor vessel inventory make up during an external flooding scenario up to

and including the probable maximum flood event which could result in reactor vessel

water level lowering below the top of active fuel. (AV 05000237/2013002-02;

05000249/2013002-02, Deficiency In Abnormal Operating Procedures for Site

Response to External Flooding Events)

This finding does not represent an immediate safety concern. The licensee entered this

issue into the corrective action program as IR 1485203, NRC Question Regarding

External Flooding. Corrective actions completed include, implementation of a TSG-3,

Attachment T, as of November 21, 2012, for reactor vessel inventory make up with the

diesel flood pump and revising DOA 0010-04 requiring operators to isolate the reactor

recirculation loops in order to minimize reactor coolant system leakage.

The inspectors intend on observing the licensees additional modifications and

simulations of the flood strategy and the maintenance and control of flood strategy

equipment through the annual external flooding inspection sample as governed by

Inspection Procedure 711111.01, Adverse Weather Protection.

.4 Selected Issue Follow-Up Inspection: Corrective Actions Following Identification of a

Potential Non-conservative Technical Specification

a. Inspection Scope

The inspectors reviewed plant design analysis and licensee actions to correct a potential

non-conservative technical specification. Technical Specification 3.6.2.5, Drywell to

Suppression Chamber Differential Pressure, potentially did not address design basis

accident impacts on the containment. Following a Safety Communication from General

Electric in July 2002, the licensee determined that TS 3.6.2.5 was potentially non-

conservative in that the limiting condition for operations (LCO) action did not establish

plant conditions which addressed the effects on containment of a design basis loss of

coolant accident (LOCA). Specifically, in August 2002, the licensee implemented the

administrative controls of NRC Administrative Letter 98-10, Dispositioning of TSs that

are Insufficient to Ensure Plant Safety, for maintaining adequate differential pressure

between the drywell and the suppression pool (torus). Subsequent to establishing

administrative controls, the licensee has not submitted a license amendment to address

the technical specification.

This review constituted one in-depth problem identification and resolution sample as

defined in IP 71152-05.

b. Observations

On July 26, 2002, General Electric published Safety Information Communication

SC02-10, Drywell-to-Wetwell Differential Pressure Control TS for Some Mark I

Containments, in which it was discussed that BWR with Mark I containments requiring a

differential pressure of at least 1 psid between the drywell and the torus could be at risk

due to the effects of pool swell loads during a design basis LOCA. Specifically, if the

1 psid differential pressure was not maintained, excessive water columns would form in

the downcomer lines in the torus increasing the severity of pool swell loading on the

containment during a design basis LOCA event. The Safety Communication also noted

that the governing TS, TS 3.6.2.5, for plants with Improved Standard TSs allowed for

continued operation for 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> with differential pressure conditions less than 1 psid

34 Enclosure

and then required the licensee to lower reactor power below 15 percent rated thermal

power (RTP) within 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />. This subsequent step of reducing power below 15 percent

RTP does not address the concern of a pressure surge in the drywell, resulting from a

LOCA, driving water in the downcomer vents into the torus and creating excessive swell

loading. Reactor pressure and temperature would remain constant when power was

reduced below 15 percent RTP and as a result the drywell pressure conditions driving

the water columns would be unaffected by the power change. In order to remove the

driving force of the LOCA event on containment when differential pressure could not be

maintained greater than 1 psid, the reactor coolant system would need to be cooled and

depressurized.

Following this safety communication, the licensee took administrative actions

establishing an Operations Standing Order, Unit 2/3 Standing Order 02-05, on

August 14, 2002, which required placing the affected unit in Mode 3 (hot shutdown)

within 55 hours6.365741e-4 days <br />0.0153 hours <br />9.093915e-5 weeks <br />2.09275e-5 months <br /> and Mode 4 (cold shutdown) within 79 hours9.143519e-4 days <br />0.0219 hours <br />1.306217e-4 weeks <br />3.00595e-5 months <br /> of entering Condition B of

TS 3.6.2.5 which itself required reducing power below 15 percent RTP within 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> of

entry. In October 2002, the license performed a bounding analysis to determine an

acceptable allowed outage time based on the frequency of a seismically induced LOCA.

This analysis was used in establishing Technical Requirements Manual (TRM) 3.6.c,

Drywell-to-Suppression Chamber Differential Pressure which replaced Operations

Standing Order 02-05 in October 2003. Section 3.6.c of the TRM required in part, that if

drywell to torus differential pressure cannot be restored to greater than 1 psid within

67 hours7.75463e-4 days <br />0.0186 hours <br />1.107804e-4 weeks <br />2.54935e-5 months <br />, the affected unit must placed in Mode 3 in 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> and Mode 4 within

36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />. This procedure remains in effect at the time of writing this report. Based on

the incorrect assumption that the Boiling Water Reactor Owners Group (BWROG) was

going to review this generic issue and recommend industry wide actions, the licensee

failed to submit a license amendment request regarding the potentially non-conservative

TS 3.6.2.5 and has operated with administrative controls in place since August 2002.

The inspectors noted the licensee performed a Plant Unique Analysis Report (PUAR) in

May 1983 in response to NUREG 0661, Mark I Containment Long-Term Program. In

this analysis the licensee calculated stresses on the torus and piping and components

within the torus during a design basis LOCA under differential pressure conditions of

greater than 1 psid and zero psid. In both instances, the stress and pressure values

determined were well within the structural capacity of the torus and the components

within it. This PUAR was reviewed and accepted by the NRC as documented by Safety

Evaluation By the Office of Nuclear Reactor Regulation Related to Mark I Containment

Long-Term Program Pool Dynamic Loads Review Commonwealth Edison Company

Docket Numbers 50-237/249, dated September 18, 1985. With this approved analysis

on record, the inspectors determined that TS 3.6.2.5 was not non-conservative as the

site maintains an approved design analysis showing that even under zero differential

pressure conditions in the containment at the initiation of a design basis accident, the

containment would not be adversely affected. The inspectors determined that the

actions of TS 3.6.2.5 were ineffective in addressing the design basis behind the

existence of the requirement to maintain a differential pressure between the drywell and

the torus and was potentially in conflict with licensees TRM 3.6.c actions. The licensee

has entered this condition into its corrective action program as IR 117545 and is

considering submitting a License Amendment Request to address this specification.

35 Enclosure

4OA3 Follow-Up of Events and Notices of Enforcement Discretion (71153)

.1 Unit 3 Downpower Due to Bearing Number 11 High Temperature

a. Inspection Scope

The inspectors reviewed the licensees response to degrading conditions on Unit 3 main

turbine bearing no. 11 first identified on January 27, 2013. At approximately 0530, main

control room operators noted the start of an increasing trend in bearing no. 11

lubricating oil temperature, metal temperature and vibrations. Bearing no. 11 is located

between the alterex exciter and the main generator supporting the Unit 3 main turbine

shaft.

As conditions worsened in the early morning hours of January 28, 2013, operators

reduced power a total of 220 MWe over the course of several hours in order to maintain

bearing temperatures below upper limits. The potential to develop AC or DC voltages in

the main turbine shaft in the vicinity of the main generator and exciter is not uncommon

and is normally mitigated by grounding brushes which are tensioned in contact with the

main turbine shaft. If the grounding brushes do not direct current flows to ground, then

arcing between the shaft metal and the bearing metal will begin to degrade the bearing.

The Operations personnel initial attempt to determine the status of the grounding

brushes by a visual inspection could not identify the tension with which they were

making contact with the shaft. This attempt to determine the status of the grounding

brushes delayed the licensees eventual recovery from the condition as management

believed initially that the brushes were performing their function. On the evening of

January 28, 2013, licensee electrical maintenance personnel performed troubleshooting

under Work Order 01610877-09 and discovered that the shaft grounding brushes were

not properly tensioned and corrected the condition. Bearing vibrations immediately

returned to a stable, normal value. Bearing metal and oil temperatures stabilized at a

slightly higher than normal value.

The licensee performed bearing analysis measurements with the bearing vendor and

identified that the bearing had sustained minor damage, but would be able to continue

operations at full power conditions for the remainder of the planned operating cycle. The

licensee developed and implemented a detailed adverse condition monitoring plan for

control room and field operators to perform in order to ensure bearing parameters

remain stable during the operating cycle. In addition, a root cause analysis performed

by the licensee identified that a miscommunication between licensee mechanical and

electrical maintenance staff during plant restoration coming out of refueling outage

D3R22 in December 2012 resulted in the shaft grounding brushes being installed on

their brackets without being tensioned in place. Licensee corrective actions include

revising model work orders for turbine shaft grounding equipment to include vendor

manual steps to verify correct adjustment with completion signature required.

On January 29, 2013, the licensee restored Unit 3 to full power conditions. The

inspectors observed main control room operations throughout this event, reviewed

licensee troubleshooting plans, bearing analysis results, adverse condition monitoring,

and the eventual root cause analysis.

Documents reviewed in this inspection are listed in the Attachment to this report.

This event follow-up review constituted one sample as defined in IP 71153-05.

36 Enclosure

b. Findings

No findings were identified.

4OA5 Other Activities

.1 (Closed) Unresolved Item 05000237/2011004-01; 05000249/2011004-01,

Classification of Emergency Diesel-Driven Flood Pump to Required Quality Standards

a. Inspection Scope

The inspectors reviewed the unresolved item and additional documentation provided by

the licensee regarding the safety classification status of the emergency diesel-driven

flood pump to determine the proper safety classification of the pump.

b. Findings

Introduction: The inspectors identified an unresolved item regarding the safety

classification of the emergency diesel-driven flood pump.

Description: On April 8, 2011, the inspectors observed the performance of WO 872864,

D2/3 6Y PM Emergency Diesel Pump (Flood Pump) Operation. After the surveillance

was completed, the inspectors reviewed the completed work package and identified that

the work instructions did not include acceptance criteria.

Title 10 of the Code of Federal Regulations, Part 50, Appendix B, Quality Assurance

Criteria for Nuclear Power Plants and Fuel Reprocessing Plants, establishes quality

assurance requirements for the design, manufacture, construction, and operation of

structures, systems and components that prevent or mitigate the consequences of

postulated accidents that could cause undue risk to the health and safety of the public.

The pertinent requirements of this appendix apply to all activities affecting the safety-

related functions of those structures, systems, and components.

Appendix B, Criterion XI, Test Control, requires that licensees establish a test program

to assure that all testing required to demonstrate that structures, systems, and

components will perform satisfactorily in service is identified and performed in

accordance with written test procedures which incorporate the requirements and

acceptance limits contained in applicable design documents. Hence, the inspectors

questioned whether the test procedure for testing the emergency diesel-driven flood

pump should have had acceptance criteria to demonstrate that the flood pump would

perform satisfactorily in service.

Upon further discussions with the licensee, the inspectors noticed that in early 2007,

the flood pump was reclassified as non-safety-related. Based on the definition of

safety-related systems, structures and components, as described in 10 CFR 50.2,

Definitions, and based on the fact that the flood pump is utilized to mitigate the

consequences of an event described in Section 3.4.1.1, External Flood Protection

Measures, of the Dresden UFSAR, the inspectors were concerned that the flood pump

had been misclassified as non-safety and it should have been classified as a

safety-related piece of equipment. The licensee was unable to produce documentation

that explained the rationale behind the safety downgrade.

37 Enclosure

Upon further evaluation, the inspectors determined that flooding cannot be considered a

Design Basis Event because Dresdens original license was issued describing the plant

as a dry site. Even though the full term license for Unit 2 was issued incorporating the

Systematic Evaluation Program (SEP) requirement for a Flooding Emergency Plan, the

SEP did not require any backfits. The Emergency Flood Plan is a license requirement

because it was incorporated into the Full Term Operating License for Unit 2. Therefore,

since flooding is not a Design Basis Event, the emergency diesel-driven flood pump

would not be required to be safety-related.

This Unresolved Item is closed.

4OA6 Management Meetings

.1 Exit Meeting Summary

On April 8, 2013, the inspectors presented the inspection results to Mr. D. Czufin, and

other members of the licensee staff. The licensee acknowledged the issues presented.

The inspectors verified that no proprietary information was retained by the inspectors or

documented in this report.

.2 Interim Exit Meetings

Interim exits were conducted for:

  • The inspection results for the areas of radiological hazard assessment and

exposure controls; and radioactive gaseous and liquid effluent treatment with

Mr. S. Marik, Plant Manager, on February 1, 2013.

  • The preliminary White determination for the finding associated with the plants

flooding response procedure with Mr. S. Marik on April 19, 2013.

The inspectors confirmed that none of the potential report inputs discussed were

considered proprietary.

ATTACHMENT: SUPPLEMENTAL INFORMATION

38 Enclosure

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

D. Czufin, Site Vice President

S. Marik, Station Plant Manager

J. Biegelson, Engineering

H. Bush, Radiation Protection Manager

J. Cady, Radiation Protection Manager

P. Chambers, Dresden Licensed Operator Requalification Training Lead

P. DiSalvo, GL 89-13 Program Owner

H. Do, Corporate ISI Manager

D. Doggett, Emergency Preparedness Manager

H. Dodd, Regulatory Assurance Manager

J. Fox, Design Engineer

D. Glick, Radioactive Material Shipping Specialist

G. Graff, Nuclear Oversight Manager

M. Hosain, Site EQ Engineer

R. Johnson, Chemist RETS/ODCM

B. Kapellas, Operations Director

D. Ketchledge, Engineering

J. Knight, Director, Site Engineering

M. Knott, Instrument Maintenance Manager

J. Kish, Site ISI

S. Kvasnicka, NDE Level III

D. Leggett, Chemistry Manager

T. Mohr, Supervisor, Engineering Programs

P. Mankoo, Radiation Protection

G. Morrow, Shift Operations Superintendent

M. McDonald, Maintenance Director

T. Mohr, Programs Engineering Manager

P. OBrien, Regulatory Assurance - NRC Coordinator

D. OFlanagan, Security Manager

M. Otten, Operations Training Manager

R. Ruffin, Licensing Engineer

J. Sipek, Work Control Director

R. Sisk, Buried Pipe Program Owner

L. Torres, Engineering

Nuclear Regulatory Commission

J. Cameron, Chief, Division of Reactor Projects, Branch 6

L. Kozak, Senior Risk Analyst

IEMA

R. Zuffa, Illinois Emergency Management Agency

1 Attachment

ITEMS OPENED, CLOSED AND DISCUSSED

Opened

05000237/2013002-01 FIN Failure to Include Adequate Acceptance Criteria in a

05000249/2013002-01 Surveillance Test (1R01.3)05000237/2013002-02 AV Deficiency In Abnormal Operating Procedures for Site

05000249/2013002-02 Response to External Flooding Events (Section 4OA2.3)

Closed

05000237/2013002-01 FIN Failure to Include Acceptance Criteria in a Surveillance

05000249/2013002-01 Test. (1R01.3)05000237/2011003-01 URI Failure to Include Adequate Acceptance Criteria in a

05000249/2011003-01 Surveillance Test (1R01.3)05000237/2011004-01 URI Classification of Emergency Diesel-Driven Flood Pump to

05000249/2011004-01 Required Quality Standards (4OA5)

Discussed

05000237/2004010-02 NCV Source of Make-up Water (1R01.3)05000249/2004010-02

05000237/2006010-04 URI Full Flow Testing of the Diesel Driven Flood Pump at

05000249/2006010-04 Design Conditions (1R01.3) URI was closed in

IR 05000237/2007003, 05000249/2007003

05000237/2007003-04 NCV Failure to Identify and Correct Issues with the Operation

05000249/2007003-04 and Testing of the Diesel Driven Pump Used to Respond

to External Flooding (1R01.3)

2 Attachment

LIST OF DOCUMENTS REVIEWED

The following is a partial list of documents reviewed during the inspection. Inclusion on this list

does not imply that the NRC inspector reviewed the documents in their entirety, but rather that

selected sections or portions of the documents were evaluated as part of the overall inspection

effort. Inclusion of a document on this list does not imply NRC acceptance of the document or

any part of it, unless this is stated in the body of the inspection report.

1R01 Adverse Weather Protection (71111.01)

- OP-AA-108-107-1001, Station Response to Grid Capacity Conditions, Revision 4

- OP-AA-102-102, General Areas Checks and Operator Field Rounds, Revision 12

- IR 1465907, NRC Senior Resident Question

1R04 Equipment Alignment (71111.04)

- DOP 1300-M1/E1, Unit 2 Isolation Condenser System, Revision 17

- Drawing M-28, Diagram of Isolation Condenser Piping

- NRC Inspection Report 05000219/2012005, 10/01/2012 - 12/31/2012; Exelon Energy

Company, LLC, Oyster Creek Generating Station

- Exelon Oyster Creek Procedure 2400-GMM-3900.52

- IR 1487125, U2 Isolation Condenser Support Nut Engagement Deficiency

- DOP 1300-M1/E1, Unit 3 Isolation Condenser, Revision 23

- WO 1571975-13, Weld Map for HPCI Drain Line Replacement of Chrome-Moly Piping with

Stainless Steel Pipe

- DOP 2300-M1/E1, U2 HPCI System Checklist, Revision 38

- Drawing M-51, Diagram of High Pressure Coolant Injection Piping

- SA-AA-141, Management & Control of Hexavalent Chromium During Welding, Cutting, and

Grinding Activities, Revision 1

1R05 Fire Protection (71111.05)

- CALCULATION: DRE97-0105, Determination of Combustible Loading, Revision 8

- Dresden Station Units 2 and 3, Commonwealth Edison Company, Fire Protection Reports,

Volume 4, Interim Measures/Exemption Requests, Section 3.5, Justification for Lack of

Complete Detection and Suppression in Fire Area TB-II.

- Dresden Station Units 2 and 3, Commonwealth Edison Company, Fire Protection Reports,

Volume 1, Updated Fire Hazards Analysis

- Dresden Station Units 2 and 3, Commonwealth Edison Company, Fire Protection Reports,

Volume 4, Interim Measures/Exemption Requests, Section 3.5, Justification for Lack of

Complete Detection and Suppression in Fire Area RB2-II

- IR 1485984, NRC Question on Fire Protection

- IR 1485977, Fire Protection - Pre-Fire Plans

1R06 Flooding (71111.06)

- WO 01505382, Need WR: U3 CCSW VLT Drain CHK VLV Replace with SR Comp.

- WO 01297399-01, D3 8Y PM Perform Check Valve Inspection 3-4999-75

- IR 1477386, Threaded Elbow Degraded and in Need of Replacement

- IR 1477499, Slow Draining During Performance of DOS 4400-01

3 Attachment

1R11 Licensed Operator Requalification Program (71111.11)

- IR 1467190, Apparent Cause Report - Dresden High Exam Failure Rate During LORT Cycle

Exam

1R12 Maintenance Effectiveness (71111.12)

- IR 1448857, Request Design Engineering to Review HELB Barriers for MRule

- IR 1486451, NRC Identified Editorial Error in MRULE A3 Assessment

- Maintenance Rule Periodic Assessment no.9 (10CFR50.65(a)(3) Assessment) Assessment

Period 10/1/2010 - 9/30/2012

- DES 6700-09, Revision 23, Inspection and maintenance of General Electric MC-4.76

Horizontal Draw-out Metal Clad Switchgear

- MA-DR-067-002, Circuit Breaker Control Revision 0

- MA-DR-725-113, Inspection and Maintenance of General Electric 4 KV Magne-Blast Circuit

Breakers Types AMH4.76-250 (Horizontal Drawout), Revision 04

- MA-DR-773-302, Dresden Standby Diesel Generator 2 and 4 KV ACB 2422 Control Circuit

Checks Revision 09

- IR 1374783, Maintenance Rule Function Z67-3 At Risk

- IR 1364609, Result of 4KV BKR Delayed Closing Failure Analysis Report

- IR 1303972, 4KV Breaker Cubicle MOC Switch Parts Issues

- IR 1282685, Breaker Did Not Reclose in Test Position During Surveillance

- IR 1281382, Potentially Deficient Prop Spring Bracket hardware 4KV BKR

- IR 1280299, 4KV Cubicle MOC Switch Rubber Bumper Degrading (New)

- IR 1251072, 1-6712-8, Main Feed to Bus 15 from Bus 12 BRKR Will Not Close

- IR 1216097, HCCT no.3 Pump Motor Breaker Will Not Rack In

- IR 1191551, 4KV Merlin Gerin Circuit Breaker B Phase Bottle Cracked

- IR 1472026, Over Voltage Relay Flag Is Up

- IR 1437824, 4KV Breaker UTC 2861736 Does Not Charge Consistently

- IR 1361972, Results of Troubleshooting, 4KV Breaker Charging Motor

- IR 1399081, NRC Concern - Historical Operability for 2A CCSW PP Breaker

- IR 13339668, Product Advisory Letter Not Incorporated Into Breaker Insp.

- IR 1232355, Streamline 4160V Breaker Trip/Close Fuse Replacements

- IR 1280668, Bus 23 Undervoltage Load Shed

- WO 1064044, 16Y PM Overhaul 4KV Breaker UTC 997129

- IR 1482952, Engineering Requests ACE - 125VDC PCM Template

- IR 1437844, TS Required Paperwork Not Submitted for Record Retetention

- IR 1443849, Feed Breaker Not Operating Properly D3R22SU

- IR 1471251, 2D LPCI Pump Breaker Will Not Charge Springs

- IR 1477941, MRULE: 4KV Breaker Performance Criteria is Non-Conservative

- IR 1443228, MRULE: System 67, MPFF is a RMPFF

- IR 1441171, Bus 33 CUB 10, Bus 33-1 Feed Breaker Wont Close

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

- OP-AA-108-117 Rev.3

- IR 1478889, NRC Inspector Questioned Shift on PPW for SBLC

- Ops Policy 02, Attachment B - Protected Equipment List

4 Attachment

1R15 Operability Determinations and Functional Assessments (71111.15)

- Calculation DRE98-0030, Rev. 0, Determination of Setpoint of CST Low-Low Level Switches

to Prevent Potential Air Entrainment form Vortexing During HPCI Operation.

- IR 1453700, Key Calc Review Identifies Issues in DRES98-0030

- EC 391829, Evaluation of Issues Identified in Calculation DRE98-0030, Revision 0

- EC 360021, Reroute of the Buried HPCI Cross-Tie Piping, Revision 1

- Drawing M-197, Sheet 11 Piping Isometric HPCI Cross-Tie 2/3-3327A-16

- Drawing M-197, Sheet 1 Outdoor Piping

- WO 01575845, Dresden 3 Quarterly Technical Specification HPCI Motor Operated Valve

Operability Surveillance, Revision 1

- IR 1455933, U3 HPCI Valve Found in Alert Range During Valve Timing

- Drawing M-347. Diagram of Reactor Feed Pump

- Drawing M-374, Diagram of High Pressure Coolant Injection Piping

- ER-AA-321, IST Valve Evaluation Form, Revision 12

- Dresden Updated Final Safety Analysis Report (UFSAR), Section 5.2.5, Detection of Leakage

Through Reactor Coolant Pressure Boundary

- IR 128973, NRC Drywell closeout inspection items

- OP-DR-108-111-1003, Drywell Leakage Troubleshooting, Revision 03

- DOS 1600-29, Unit 2 and 3 Drywell Temperature Surveillance, Revision 5

- DAN 902(3)-5 F-3, Rod Drive Temp Hi, Revision 15

- DAN 902(3)-4 C-17,Drywell Equip Sump Temp Hi, Revision 8

- IR 1487125, U2 Isolation Condenser Support Nut Engagement Deficiency

- IR 1487131, U3 Isolation Condenser Support Nut Engagement Deficiency

- MA-MW-736-600, Torquing and Tightening of Bolted Connections, Revision 5

- Drawing ISI-201, Inservice Inspection Class II Isolation Condenser Piping

- Drawing ISI-206, Inservice Inspection Class II Isolation Condenser Piping

- Drawing ISI-307, Inservice Inspection Class III Isolation Condenser and Vent Piping

- Drawing ISI-305, Inservice Inspection Class III Isolation Condenser and Vent Piping

- Drawing Hanger M-1163D-553

- Drawing Hanger M-1199D-1022

- Drawing Hanger M-1199D-1023

- Drawing Hanger M-1199D-1024

- Drawing Hanger M-1163D-554

- Drawing Hanger M-1163D-555

- EC 388891, 2013: Unit 2 SR 480V Bucket Replacement Project, Revisions 0 and 1

1R18 Plant Modifications (71111.18)

- 50.59 Screening No. 2013-0064, Unit 3 Main Steam Line Isolation Valve Closure Scram

Circuit Functional Test

- Drawing 12E-3466, Schematic Diagram Reactor Protection System Channel B Scram &

Auxiliary Trip Relays, Sheet No. 1

- Drawing 12E-3464, Schematic Diagram Reactor Protection System Channel B Trip Aux.

Relays, Sheet No. 2

- IR 1484861, U3 C Main Steam Line Limit Switch Failure

- DOS 0500-27, Unit 3 main Steam Line Isolation Valve Closure Scram Circuit Functional

Test, Revision 1

5 Attachment

1R19 Post-Maintenance Testing (71111.19)

- IR 1465026, Broken Motor Cooling Blades

- WO 1418376, Dresden Unit 2 Two Year PM Standby Diesel Generator Inspection

- IR 1475119, Re-occurring Unexpected Unit 2 EDG Alarm, February 14, 2013

- DOS 6600-01, Diesel Generator Surveillance Tests, Revision 122

- WO 1605861, D2 Quarterly TS HPCI Pump Operability Test and IST Surveillance

- IR 1488336, NRC Identified Housekeeping Issues in the U2 HPCI Room

- WO 1423633, D3 2Y TS HPCI Pump Comprehensive Oper Test and IST Surv

- IR 1490995, Unexpected Alarm HPCI Room Sump Level High

- IR 1492807, Newly Replaced Valve Leaks Past Seat for D2/3 EDG

- WO 1424316-03, D2/3 2 year PM Diesel Generator Engine Temperature Instrument CAL -

Check for Leaks

- WO 681423, D2/3 4year Inspect Cubicle 3 at Bus 40 (Bus Tie to Bus 23-1) - Perform PMT on

Bus 40C

- DOS 6600-01, Diesel Generator Surveillance Tests, Revision 122

1R22 Surveillance Testing (71111.22)

- DOS 1500-10, LPCI System Pump Operability and Quarterly Test with Torus Available and

Inservice Test, Revision 67

- DIS 1500-09, Revision 19, LPCI Reactor Recirculating Pump A and B Differential Pressure

Indicating Switch Calibration and Channel Functional Test

- IR 1462734, Data Transfer Error Discovered During Review of DIS 1500-09

- IR 1461469, Old Word Perfect Symbol Caused < or = to become > or =, January 11, 2013

- Drawing M-357, Sheet 2, Diagram of Nuclear Boiler & Reactor Recirculating Piping

- Drawing 12E-3437A, Schematic Diagram LPCI Containment Cooling System

- Drawing 12E-3438A, Schematic Diagram LPCI Containment Cooling System

- DOP 2000-180, Drywell Sump Operation With Unit On-Line, Revision 04

- Appendix A, Unit Daily Surveillance Log, Attachment A, Eight Hour Shifts, Revision 129

- DES 0040-02, 600 Volt Butyl Cable EQ Surveillance, Revision 10

- DFPS 4123-05, 2/3 Diesel Fire Pump Operability, Revision 50

- Electrical Drawing 12E-2750A, Sheet 1, Wiring Diagram Feedwater and Recirculation

Panel 9

- Electrical Drawing 12E-2424, Sheet 1, Schematic Diagram Recirculating Pump Speed

Control

- WO 1396238, D2 2Y PM&C Recirc Flow Dual Limiter 262-26B

- WO 1579759, D2 QTR TS LPCI System Pump Run and IST Surveillance

1EP6 Drill Evaluation (71114.06)

- IR 1472861, EP DEP Failure During TSC Focus Area Drill, February 8, 2013

- IR 1474238, NOS ID: DEP Failures Identified as Level 4 Issue Reports, February 12, 2013

2RS1 Radiological Hazard Assessment and Exposure Controls (71124.01)

- RWP 10014505; 2013 Radwaste Concentrated Waste Vault Sludge Removal; Revision 0

- Unit 2/3 Radwaste EL 517 Reboiler Area Survey Map; January 8, 2013

- Unit 2/3 Radwaste EL 517 Reboiler Area Survey Map; January 16, 2013

- Unit 3 reactor 570 Fuel Pool Cleanup Pump/Heat Exchanger Area; January 8, 2013

6 Attachment

- RWP 10014505; 2013 Radwaste Concentrated Waste Vault Sludge Removal; WO 1221622;

Vacuum Vessel Full Sludge from the Concentrated Waste Vault; ALARA Plan; January 29,

2013

- RWP 10014505; 2013 Radwaste Concentrated Waste Vault Sludge Removal; Barnhart to

Remove Floor Plugs in the B Concentrator Vault for Prep of the CW Vault; January 24, 2013

- RWP 10014505; 2013 Radwaste Concentrated Waste Vault: Decon Area Remove Misc Bags

and Parts from Area at 517 Reboiler; ALARA Briefing Checklist RP-AA-401

2RS6 Radioactive Gaseous and Liquid Effluent Treatment (71124.06)

- CY-DR-170-220; Revision 5; Unit 2 and 3 Reactor Building Vent Noble Gas Sampling;

January 31, 2013

- DIS-1700-14; Unit2/3 Reactor Building Vent Stack SPING Calibration; November 2, 2012

- RP-AA-605; Waste Stream Results Review Part 61; May 11, 2012

- R-01398192; Document Request of the Licensees Process Monitor Setpoint Bases;

August 7, 2012

- DIS-1700-14; Unit2/3 Main Chimney SPING Calibration; February 2, 2012

- DIS-1700-14; Unit2/3 Main Chimney SPING Calibration; February 19, 2012

- WC-AA-104;Quarterly Tech Spec Reactor Building Vent Radiation Monitor Calibration and

Functional Tests; January 24, 2013

- L53233; Teledyne Brown; Report of Analysis/Certificate of Conformance; Waste Surge Tanks

Sampling Wells; January 15, 2013

- L533074; Teledyne Brown; Report of Analysis/Certificate of Conformance; Steam Dryer

Mausoleum Sampling Wells; January 30, 2013,

- AR-01322619; Unable to Complete Sample Line Inspection for Chimney SPING; February 3,

2012

- AR-01322619; Engineering Evaluation for Visual Inspection of Sample Lines from the SPING

to Chimney; March 23, 2012

- WO 1337345; 24 Month Tech Spec.(TS) Reactor Building Vent Sampler Flowmeter

Calibration; May 5, 2012

- WO 1575796; D3 Quarterly TS Reactor Vent Radiation Monitor Calibration and Functional;

December 20, 2012

- WO 1236618; D3 TS Reactor Building Vent Sampler Flowmeter Calibration; April 15, 2011

- AR-01305481; D2/3 Main Chimney SPING not Responding During Calibration; February 4,

2012

- AR-01329443; Unexpected Alarm on the Liquid Process Rad Monitor; February 12, 2012

- AR-01330334; Liquid Process Rad Monitor Downscale; February 22, 2012

- AR-01397142; Liquid Process Rad Monitor Alarms on Unit-2 and Unit-3; August 4, 2012

- AR-01392741; HPGE Detector Failed Multiple Performance Checks; July 27, 2012

- AR-01392819; Out of Calibration RP Instrument Found in Plant; July 25, 2012

4OA1 Performance Indicators (71151)

- NEI 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6

- Unit 2 and 3 Performance Indicator data for First through Fourth Quarter 2012

4OA2 Identification and Resolution of Problems (71152)

- EP-AA-1004, Radiological Emergency Plan Annex For Dresden Station, Revision 29

- IR 1453073, NRC Question on TSG 3 Strategies

- IR 1469502, CDBI-2013 IC Diesel Makeup Pump Building Foundation Buoyancy

7 Attachment

- IR 1485203, NRC Question Regarding External Flooding

- IR 1482141, EC 391644 Approved Prior to Affected Calculation Approval

- EP-AA-1004, Exelon Nuclear Radiological Emergency Plan Annex For Dresden Station,

Revision 29

- DOA 0010-04, Floods, Revision 32

- DOA 0010-04, Floods, Revision 37

- Calculation DRE01-030, Probable Maximum Flood Effects at the ISFSI Pad, Revision 0

- Drawing M-23 Sheet 3, Diagram of Fire Protection Piping

- Drawing M-33, Diagram of Standby Liquid Control Piping

- TSG-3, Operational Contingency Action Guidelines, Revision 10

- TSG-3, Attachment H, RPV Injection Using Portable Diesel Driven Pump

- TSG-3, Attachment T, Provide RPV Make Up From Fire Protection System Via SBLC

- COM-02-041-2, Plant Unique Analysis Report Volume 2, Suppression Chamber Analysis,

Revision 0, May 1983

- SC02-10, GE Nuclear Energy Safety Communication, Drywell-to-Wetwell Differential

Pressure Control Technical Specification for Some Mark I Containments, July 26, 2002

- SA-1115, Significance of Seismic-Induced LOCAs at Dresden, Revision 1

- OP-AA-102-104, U2/3 Standing Order, Tech Spec LCO 3.6.2.5 Supplemental Administrative

Actions, Revision 0

- Commitment Letter from Commonwealth Edison to Mr. Paul OConnor, SEP Topic II-3.B,

Flooding Potential and Protective Requirements; II-3.B.1, Capability of Operating Plants to

Cope with Design Basis Flood Conditions; and II-3.C, Safety Related Water Supply (Ultimate

Heat Sink), Dated November 17, 1982

- Letter from NRC to Licensee, Request for a Written Response to NRC Observations and

Concerns Regarding Dresden Station Response Plan for External Flooding Events, Dated

November 1, 2012

- Letter from Mr. David Czufin to NRC, Response to NRC Request for a Written Response to

NRC Observations and Concerns Regarding Dresden Station Response Plan for External

Flooding Events, Dated December 1, 2012

- Letter from NRC to Licensee, Acknowledgement of Response to NRC Request for a Written

Response to NRC Observations and Concerns Regarding Dresden Response Plan for

External Flooding Events, Dated January 3, 2013

- Letter from Mr. David Czufin to NRC, Response to Acknowledgement of Response to NRC

Request for a Written Response to NRC Observations and Concerns Regarding Dresden

Response Plan for External Flooding Events, Dated January 31, 2013

- GE Safety Information Communication, Drywell to Wetwell Differential Pressure Control

Technical Specification for Some Mark I Containments, July 26, 2002

- Letter from J. Henry, Evaluation of Entry Into Technical Specification Limiting Condition of

Operation 3.6.25 for Drywell to Suppression Chamber Differential Pressure, October 16, 2002

- IR 117545, DW to Torus DP Control Tech Spec for a Mark I Containment

- 50.59 Screening Form, TRM 3.6 C, 2003-0349, Revision 0

- IR 1490293, De-energized Relay Picked Up

- Letter from NRC to Licensee, Mark I Containment Long Term Program, dated

September 18, 1985

4OA3 Follow Up of Events and Notices of Enforcement Discretion (71153)

- IR 1467631, Unexpected Alarm; 903-8 E-12 U3 Gen/Exc Ground

- IR 1468057, U3 Turbine Shaft Grounding Brushes Found Not Fully Tensioned

- IR 1468569, Follow-Up Actions for Unit 3 Bearing no. 11 Issue

8 Attachment

- IR 1468765, U3 Exciter BRG no. 11 Lube Oil Flow Measurement Not Accurate

- Root Cause Report 1468057-04, Unit 3 Bearing 11 Rising Vibration, Oil & Metal

Temperatures due to Work Order Referenced Vendor Manual Steps without Requiring Step by

Step Worker Sign Offs

- OP-AA-108-111, Unit 3 Bearing 11 Metal Temperature and Vibration, Revision 1

9 Attachment

LIST OF ACRONYMS USED

AC alternating current

ADAMS Agencywide Document Access Management System

ALARA As-Low-As-Reasonably-Achievable

AOP Abnormal Operating Procedure

ASME American Society of Mechanical Engineers

AV Apparent Violation

BWR Boiling Water Reactor

CAP Corrective Action Program

CCSW Containment Cooling Service Water

CDF Core Damage Frequency

CFR Code of Federal Regulations

CRD Control Rod Drive

DC direct currnet

DOA Dresden Abnormal Operating Procedure

DRP Division of Reactor Projects

EAL Emergency Action Level

ECCS Emergency Core Cooling System

EDG Emergency Diesel Generator

FIN Finding

FLEX Diverse and FLEXIBLE equipment availability program

HPCI High Pressure Coolant Injection

IC Isolation Condenser

IMC Inspection Manual Chapter

INPO Institute of Nuclear Power Operations

IP Inspection Procedure

IR Inspection Report

IR Issue Report

ISI Inservice Inspection

JLD Japan Lessons Learned

LCO Limiting Condition for Operation

LOCA Loss of Coolant Accident

LLC Limited Liability Corporation

LORT Licensed Operator Requalification Training

LPCI Low Pressure Coolant Injection

MSL Mean Sea Level

NCV Non-Cited Violation

NEI Nuclear Energy Institute

NRC U.S. Nuclear Regulatory Commission

OCA Owner Controlled Area

PARS Publicly Available Records System

PI Performance Indicator

PM Planned or Preventative Maintenance

PMF Probable Maximum Flood

PMT Post-Maintenance Testing

psid pounds per square inch differential

psig pounds per square inch gauge

PUAR Plant Unique Analysis Report

RP Radiation Protection

10 Attachment

RPV Reactor Pressure Vessel

RTP Rated Thermal Power

SBLC Standby Liquid Control

SDP Significance Determination Process

SEP Systematic Evaluation Program

SERP Significance and Enforcement Review Panel

SSC Systems, Structures, and Components

SRA Senior Risk Analyst

TAF Top of Active Fuel

TS Technical Specification

TSG Technical Support Guidance

UFSAR Updated Final Safety Analysis Report

URI Unresolved Item

Vdc Volts direct current

WO Work Order

11 Attachment

M. Pacilio -2-

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its

enclosure, and your response (if any) will be available electronically for public inspection in

the NRC Public Document Room or from the Publicly Available Records System (PARS)

component of NRC's Agencywide Document Access and Management System (ADAMS).

ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html

(the Public Electronic Reading Room).

Sincerely,

/RA by Kenneth G. OBrien for/

Steven A. Reynolds, Director

Division of Reactor Projects

Docket Nos. 50-237, 50-249

License Nos. DPR-19 and DPR-25

Enclosure: Inspection Report 05000237/2013002, 05000249/2013002

w/Attachment: Supplemental Information

cc w/encl: Distribution via ListServ

DOCUMENT NAME: G:\DRPIII\Dres\DRES 2013 002.docx See Previous Concurrence

Publicly Available Non-Publicly Available Sensitive Non-Sensitive

To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl "E" =

Copy with attach/encl "N" = No copy

OFFICE RIII RIII RIII RIII RIII

NAME JRutkowski:dtp JCameron LKozak SOrth*PL for SReynolds

  • KGO for

DATE 04/25/13 04/25/13 04/25/13 04/30/13 04/07/13

  • OE and NRR concurrence on 4/29 via e-mail

OFFICIAL RECORD COPY

Letter to M. Pacilio from J. Cameron dated May 7, 2013.

SUBJECT: DRESDEN NUCLEAR POWER STATION, UNITS 2 AND 3, INTEGRATED

INSPECTION REPORT 05000237/2013002, 05000249/2013002

DISTRIBUTION:

Doug Huyck

RidsNrrDorlLpl3-2 Resource

RidsNrrPMDresden Resource

RidsNrrDirsIrib Resource

Chuck Casto

Cynthia Pederson

Steven Orth

Allan Barker

Christine Lipa

Carole Ariano

Linda Linn

DRPIII

DRSIII

Patricia Buckley

Tammy Tomczak

ROPreports.Resource@nrc.gov