ML20216E212

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Revised MOR for Jan 1998 for Prairie Island Nuclear Generating Plant for Unit 2 & Narrative Summary of Operating Experience
ML20216E212
Person / Time
Site: Prairie Island  Xcel Energy icon.png
Issue date: 01/31/1998
From: Dugstad D
NORTHERN STATES POWER CO.
To:
Shared Package
ML20216E202 List:
References
NUDOCS 9803170444
Download: ML20216E212 (3)


Text

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Corrected report due to meter reading problems caused by newly installed digital meters.

This changed values for Unit 2's operating data report, page 7*

l line numbers 17,18,21 and 22 l

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  • PRINTED 02/13/98 l*.
  • NRC MONTHLY REPORT Page5 l

! DOCKET NO. 50-306 UNIT PRAIRIE ISLAND NO. 2 l DATE 02/13/98

[ COMPLETED BY' DALE DUGSTAD TELEPHONE 612-388-11214376 NARRATIVE

SUMMARY

OF OPERATING EXPERIENCE MONTH: JANUARY 1998 During the rnonth of January Unit 2 was base loaded.

On the 22nd leakage of the Reactor Coolant System was found to be increasing. On Friday, January 23, during a containment inspection, Part Length Control Rod drive mechanism at location G9 was found to be leaking. The Generator was taken off-line on the 24th at 1522 and the Reactor was manually shutdown at 1537. Work to repair the leak was started immediately.

The Unit remained in this outage through the rest of the month.

This ended a continuous operating run of approximately 177 days.

Note: on February 13,1998 the report was corrected due to meter reading problems caused by newly installed digital meters.

This changed values for Unit 2's operating data report, page 7, line numbers 17,18,21 and 22 l

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CURRENT CONTINUOUS OPERATING RUN OF 0 DAYS

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  • NRC MONTHLY REPORT PRINTED 02/13/98 Page 7 f DOUKET NO. 50-306 UNIT PRAIRIE ISLAND NO. 2 j DATE 02/13/98 l COMPLETED BY DALE DUGSTAD TELEPHONE 612-388-11214376 OPERATING DATA REPORT OPERATING STATUS ,
1. UNIT NAME: PRAIRIE ISLAND NO. 2
2. REPORTING PERIOD: JANUARY 1998
3. LICENSED THERMAL POWER (MWT): 1650
4. NAMEPLATE RATING (GROSS MWE): 593
5. DESIGN ELECTRICAL RATING (NET MWE): 530
6. MAXIMUM DEPENDABLE CAPACITY (GROSS MWE): 544'
7. MAXIMUM DEPENDABLE CAPACITY (NET MWE): 512
8. IF CHANGES OCCUR IN CAPACITY RATINGS (ITEMS 3 - 7) SINCE LAST REPORT, GIVE REASON:

NONE

9. POWER LEVEL TO WHICH RESTRICTED, IF ANY (NET MWE): NONE
10. REASONS FOR RESTRICTIONS, IF ANY: NONE THIS MONTH YR-TO-DATE CUMULATIVE
11. HOURS IN REPORTING PERIOD 744 744 202630
12. NUMBER OF HOURS REACTOR CRITICAL 567.6 567.6 179293.8 t3. REACTOR RESERVE SHUTDOWN HOURS 0.0 0.00 1516.1
14. HOURS GENERATOR ON-LINE 567.4 567.4 177794.5
15. UNIT RESERVE SHUTDOWN HOURS 0.0 0.00 0.00
16. GROSS THERMAL ENERGY GENERATED (MWH) 932174 932174 283396761 17 GROSS ELECTRICAL ENERGY GENERATED (MWH) 316010 316010 92813420
18. NET ELECTRICAL ENERGY GENERATED (MWH) 300040 300040 87751210
19. UNIT SERVICE FACTOR 76.3 76.3 87.7
20. UNIT AVAILABILITY FACTOR 76.3 76.3 87.7
21. UNIT CAPACITY FACTOR ( MDC NET) 78.8 78.8 86.2
22. UNIT CAPACITY FACTOR ( DER NET) 76.1 76.1 81.7
23. UNIT FORCED OUTAGE RATE 23.7 23.7 2.7
24. FORCED OUTAGE HOURS 176.6 176.6 4907.7
25. SHUTDOWNS SCHEDULED OVER NEXT SIX MONTHS (TYPE, DATE, AND DURATION OF EACH): ]

N/A

26. IF CURRENTLY SHUTDOWN, ESTIMATED STARTUP DATE:

Late February to early March.