ML20132E380

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Discusses Actions Associated W/Amend Request for TSs for Rod Block Monitor at Plant,Unit 2
ML20132E380
Person / Time
Site: Fermi DTE Energy icon.png
Issue date: 12/19/1996
From: Kugler A
NRC (Affiliation Not Assigned)
To: Gipson D
DETROIT EDISON CO.
References
NUDOCS 9612230266
Download: ML20132E380 (5)


Text

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1 p t UNITED STATES 3

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j NUCLEAR REGULATORY COMMISSION WASHINGTON, D.C. 30e86 4001 '

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l ~% **** December 19, 1996 3

! Mr. Douglas R. Gipson '

! Senior Vice President i Nuclear Generation i Detroit Edison Company 6400 North Dixie Highway  !

i Newport, Michigan 48166 ,

i l l

SUBJECT:

ACTIONS ASSOCIATED WITH AN AMENDMENT REQUEST FOR THE TECHNICAL i SPECIFICATIONS FOR THE R0D BLOCK MONITOR AT FERMI 2 1 .

Dear Mr. Gipson:

j'

! On December 2, 1996, you submitted an amendment request for Fermi 2 Technical

! Specifications (TS) 3.1.4.3, Rod Block Monitor and 3.3.6, Control Rod Block

Instrumentation. In your submittal you explained that the applicability i statement in the TS needed to be changed to ensure that all fuel limits would i be met during Cycle 6 for a rod withdrawal error at power. Therefore, your r l proposed amendment would revise the applicability statement to include the  !

! entire range of conditions for which the rod block monitor should be operable.

r i In the interim, you have established administrative controls intended to '

i ensure that appropriate actions, based on the proposed revised applicability i statement, will be taken by plant personnel if one or more channels of the rod l block monitor become inoperable. The administrative controls consist of a TS

clarification in conjunction with a' statement in the Core Operating Limits 2 Report (COLR) concerning the revised applicability. The TS c7arification i states that the [ existing) TS requirements for the Rod Block Monitor shall be i applicable whenever thermal power is greater than or equal to 30% of rated i thermal power. In addition, licensed operators have received training l concerning the revised applicability of the technical specification.

l The administrative controls described in your submittal appear to direct i appropriate action by the operators if one or more channels of the rod block i monitor becomes inoperable in the operating region not currently included in

the technical specifications. Given that the administrative controls are more conservative than the existing technical specifications, the staff does not
object to the use of these controls pending the completion of our review of your amendment request. In the interim, the staff expects that you will

! maintain the administrative controls you have described in place.

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9612230266 961219 i PDR ADOCK 05000341 i p PDR I

D. Gipson <

If you have any questions concerning this issue, please contact me.

Sincerely, l <

Andrew J. Kugler, Project Manager Project Directorate III-l ,

i Division of Reactor Projects - III/IV  !

Office of Nuclear Reactor Regulation
l l- Docket No. 50-341 i

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i Mr. Douglas R. Gipson Fermi-2 Detroit Edison Company )

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John Flynn, Esquire i

Senior Attorney l Detroit Edison Company 1 2000 Second Avenue '

Detroit, Michigan 48226 Drinking Water and Radiological Protection Division 1 Michigan Department of Environmental Quality 3423 N. Martin Luther King Jr Blvd P. O. Box 30630 CPH Mailroom Lansing, Michigan 48909-8130 U.S. Nuclear Regulatory Commission Resident Inspector's Offica 6450 W. Dixie Highway Newport, Michigan 48166 Monroe Couiity Emergency Management Division 963 South Raisinville Monroe, Michigan 48161 Regional Administrator, Region III U.S. Nuclear Regulatory Commission 801 Warrenville Road ~

Lisle, Illinois 60532-4351 Peter W. Smith ,

Director, Nuclear Licensing  !

Detroit Edison Company

  • Fermi 270 TAC 6400 North Dixie Highway Newport, Michigan 48166 l

l Separaber 1996

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D. Gipson- December'19, 1996 If you have any questions concerning this issue, please contact me.

Sincerely, Original signed by Andrew J. Kugler, Project Manager Project Directorate III-1 Division of Reactor Projects - III/IV Office of Nuclear Reactor Regulation Docket No. 50-341 cc: See next page DISTRIBUTION:

Docket File  !

PUBLIC- i OGC ACRS .

PD3-1 Reading File l MJordan, RIII AVegel, RIII JRoe EAdensam (EGA1)

LPhillips MYoung, 0GC

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DATE 12/101 /96 12/03/96 12//9 /96 12/19/96'- 12//4 /96 l

' ' I OFFICIAL RECORD COPY l

D. Gipson If you have any questions concerning this issue, please contact me.

Sincerely, Andrew J. Kugler, Project Manager Project Directorate 111-1 .

Division of Reactor Projects - III/IV '

Office of Nuclear Reactor Regulation Docket No. 50-341 cc: See next page DISTRIBUTION: i Docket File PUBLIC OGC ACRS PD3-1 Reading File MJordan, RIII AVegel, RIII JRoe EAdensam (EGAl) i LPhillips '

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