ML20073J598

From kanterella
Revision as of 10:30, 27 April 2020 by StriderTol (talk | contribs) (StriderTol Bot insert)
(diff) ← Older revision | Latest revision (diff) | Newer revision → (diff)
Jump to navigation Jump to search
Significant Const Deficiency 73 Re American Bridge Reactor Containment Bldg Structural Steel Welds.Initially Reported on 830311.Next Rept Will Be Submitted by 830520
ML20073J598
Person / Time
Site: Waterford Entergy icon.png
Issue date: 04/11/1983
From: Maurin L
LOUISIANA POWER & LIGHT CO.
To: Jay Collins
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
References
10CFR-050.55E, 10CFR-50.55E, W3I83-0112, W3I83-112, NUDOCS 8304190339
Download: ML20073J598 (3)


Text

s

  • l OUISIANA / 24a DuARONDE STREET POWER & LIGHT / P O DOX 6000
  • NEW ORLEANS. LOUISlANA 70174 * (504) 366-2345

$PUSIES SYS E April 11, 1983 L v. MAunin Voce Presxtent Nuclear Operatens W3183-Oll2 Q-3-A35.07.73'}

Mr. John T. Collins, Regional Administrator, Region lV 6 \ @ !g.

U. S. Nuclear Regulatory Commission thCh' - 1,

$)j#

611 Ryan Plaza Drive, Suite 1000 Arlington, Texas 76012 \( . \k .g

SUBJECT:

Waterford SES Unit No. 3 \ '

/

Docket No. 50-382 V' Significant Construction Deficiency No. 73 -

"American Bridge RCB Structural Steel Welding Deficiencies"

Reference:

Telecon from M. A. Livesay to J. Boardman on March 11, 1983

Dear Mr. Collins,

In accordance with the requirements of 10CFR50.55(e), we are hereby providing two copies of the Interim Report of Significant Construction Deficiency No. 73.  ;

If you have any questions, please advise.

Very truly yours, 1 ~

.7 YlCacui~

L. V. Maurin LVM/ MAL:keh l Attachment 1

I cc: 1) Director 3) Mr. E. L. Blake Office of Inspection 6 Enforcement U. S. Nuclear Regulatory Commission Washington, D. C. 20555

2) Director 4) Mr. W. M. Stevenson Office of Management Information and Program Control U. S. Nuclear Regulatory Commission Washington, D. C. 20555 F304190339 030411 P,DRADOCKOSOOOg o

~ . . . . . ._

INTERIM REPORT OF SIGNIFICANT CONSTRUCTION DEFICIENCY No. 73 AMERICAN BRIDGE RCB STRUCTURE STEEL WELDING DEFICIENCIES INTRODUCTION This_ report is submitted pursuant to 10CFR50.55(e). This report describes RCB structural steel welding concerns. This problem is considered reportable under the requirements of 10CFR50.55(e).

To_the best of our knowledge it has not been reported pursuant to 10CFR21.

DESCRIPTION During record reviews and surveillance inspections of American Bridge structural welds in the Reactor Containment Building, several welding concerns were dis-covered. These concerns include insufficient veld size, cold lap, undercut, improper contour, weld spatter, unauthorized tack ~ welds, improper fit-up of shear plate and porosity. . Ongoing inspection and record review results are expected to be evaluated by Ebasco Engineering within the next 30 days.

(American Bridge demobilized from site in 1981.)

SAFETY IMPLICATIONS Some of the welds in question were made cnt structural steel that supports or ties into safety related systems. Failure of these welds could result in pos-sible degradation of these safety systems.

CORRECTIVE ACTION TAKEN Nonconformance Report W3-5805 was initiated to track'and document this deficiency.

An update or final report will be submitted May 20, 1983.

g- -

INTERIM REPORT OF SIGNIFICANT CONSTRUCTION DEFICIENCY No. 73 AMERICAN BRIDGE RCB STRUCTURE STEEL WELDING DEFICIENCIES INTRODUCTION This report is submitted pursuant to 10CFR50.55(e). This report describes RCB

-structural steel welding concerns. This problem is considered reportable under the requirements of 10CFR50.55(e).

To the best of our knowledge it has not been reported pursuant to 10CFR21.

DESCRIPTION During record reviews and surveillance inspections of American Bridge structural welds in the Reactor Containment Building,'several welding concerns were dis-covered. These concerns include insufficient weld size, cold lap, undercut :

improper contour, weld spatter, unauthorized tack welds, improper fit-up of shear plate and porosity. Ongoing inspection and record review results are expected to be-evaluated by Ebasco Engineering within the next.30 days.

(American Bridge demobilized from site in 1981.)

SAFETY IMPLICATIONS Some of the welds in question were made on structural steel that supports or ties into safety related systems. Failure of these welds could result in pos-sible degradation of these safety systems.

CORRECTIVE ACTION TAKEN Nonconformance Report W3-5805 was initiated to track and document this deficiency.

An update or final report will be submitted May 20, 1983.

i a