ML19208A802

From kanterella
Revision as of 18:33, 16 March 2020 by StriderTol (talk | contribs) (StriderTol Bot change)
(diff) ← Older revision | Latest revision (diff) | Newer revision → (diff)
Jump to navigation Jump to search
LER 79-028/03L-0:on 790902,during Surveillance Test,Control Element Assembly 43 Slipped to 100 Inches.Caused by Voltage Fluctuation in 15-volt Power Supply.Design Mod Initiated to Install Dual Power Supplies
ML19208A802
Person / Time
Site: Calvert Cliffs Constellation icon.png
Issue date: 09/13/1979
From: Davis S
BALTIMORE GAS & ELECTRIC CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19208A799 List:
References
LER-79-028-03L-01, LER-79-28-3L-1, NUDOCS 7909170504
Download: ML19208A802 (1)


Text

'

LICENSEE EVENT REPORT CcNTsOL stOC,e l l l l l l ]@ (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 7 o i 8 9 Ml0 l C l C l N l 142 l@l L6CENSEE CODE 15 0l 0 -l 0lLICENSE 0l 0NLVuER 0l 0l -l 0l 0l@l4 1L;CiNSE.a 26 l1 l1T*PE 1Jol@l l lg 57 CAT de CON T l l !@610 l 5 l0 0l0l3l1 8 j@l0 9 l0 l2 l7 l9 l@[0 l9 l1 l3 l719 j@

0 1 7 6 5c$$*CE 60 68 69 74 75 AEPORT C ATE 30 DOCKET NLY8ER EVENT DATE EVENT CEOCA6PTION AND PPOB ABLE CONSECUENCES h o 2 l At r043 while perfaming a surveillance test, control eierent assembly (CEA) I o 3 43 slipped to 100 inches. Reactor power was reduced to less than 70 percent l 0 , l at 0140 in accordance with T.S. 3.1.3.1. CEA 43 was withdrawn and leveled l I

o ., lwith its group at 0143. LER's 78-48 (U-1) and 79-24 (U-2) describe similar events. l.

0 6 l l c 7 I I l0 8 __

7 8 9 SYSTEM CAUSE CALSE lk

.ALVE lQ[j] = 80 CCCE CCOE EUBC00E COYPONENT CCCE Sv8 CODE SL'CCOE a 9 l R lB l@ l El@ [ A f g l Cl Rl Dl Rl VI Ej @ l Z l@ lZ [@ ,

7 8 9 , 10 11 12 13 18 19 20

_ SE OUt NTI AL CCCL A a '.NCE RERCRT R E \ 'J O *'

EVENT YE4R A E PC A T NO. CODE TvPE N ldj t g a RO

@ geg .

09] l_l l 0l 2 8l jfl l0l3l lL l l_

_ 21 22 23 24 :6 27 26 29 30 31 32 AC" ION GUTLAE EFFECT SNUTCCAN A TT AC HUE N T NPRO4 PR 'V E CO* tP. CO V PC P;[N T TAKEN ACTICN CN PL ANT VETHOO HOLAS SUEvt TT E D FCAVLUB. SUPPLIER  %*ANwFACTLRER lZ l@l34El@ l25B l@ l36 Zl@ l 0 l 0l 010l 37 l Ni@ lNI@ Nl@ P 3]1l4l@

33 40 41 42 43 44 47 CAUSE CESCRIPTION AND CC ARECTIVE ACTICNS h li o ITha sliored CEA is assc-ed to be the rasult of a voltace fluctuation in the 15 I i i I volt oewer surelv. A desicn codification to innrove the raliability of 'ha I i  : Isvstem bv installino dual nouer sucolies (FCR 7E-72) is to be installed durino I i 2 i the next refueline nutace. l l{ .1 l 7 8 9 80 STA N PO'.". E R OTHEM STATUS OS O AY CISCCV ERY OESCA.FTiCN ri TTI Lt_J@ l 1101 Ol@l NA I Isl@l surveillance Test i A CTi o Tv CONTENT PFLEASEO OF EELE ASE AYOUNT OF ACTIVITY LOCATaCN OF PELE ASE i e LLj @ LZJ@ NA I NA I 7 a 9 to 11 44 45 30 PE os;'.N E . E A POSLa ES

.L;5fA ~Y'E 7 0 i 0 l 0j@l Z @OESCAJT'CN NA I 7 3 3 11 12 13 30

  • JSC .NE L NM ES

. cPE4 C ESC A:PT:C '.

i- LZ l Z .zj@l NA 1 7 d 3 11 12 30

." : c r C 2 D Av a ,E T C F ACILi rv @, ,9091703C

E,f.mCN Sa,704G 4 7

9I s 3 iol to 30 f

-3, g '!A

8. s c m a C a. t v ,

. J [ '. i8[ I IIIIIIIIIIIIl5 7 E 3 0 ca o sa ;

e

" - c3vis (3))) 234-7942 9

. .e u =av:, sea P~c ;e-  ;