ML20052F200

From kanterella
Revision as of 14:28, 10 March 2020 by StriderTol (talk | contribs) (StriderTol Bot change)
(diff) ← Older revision | Latest revision (diff) | Newer revision → (diff)
Jump to navigation Jump to search
Monthly Operating Rept for Apr 1982
ML20052F200
Person / Time
Site: Palisades Entergy icon.png
Issue date: 05/07/1982
From: Peterson D, Vandenberg D
CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.)
To:
Shared Package
ML20052F197 List:
References
NUDOCS 8205120222
Download: ML20052F200 (4)


Text

OPERATING DATA REPORT DOCKET NO. 50-255

. DATE 5-7-82 COMPLETED 11Y Motormn TELEPHONE _6316 76h-8913

, OPERATING STATUS Palicades Notes

2. Reportint Period: 820h01-820h30

, 3. Licenwd Thermal Power (MW:): ?53n

4. Nameplue Rating (Gross 31We): 811_7
5. Design Electrical Rating (Net MWe): 805
6. Maximum Dependab1: Capacity (Gross MWe): *675 7 Masimum Dependable Capacity (Net MWe). *635
5. If Changes Occur in Capacity Ratings (items Number 3 Through 7) Since Last Report.Gise Reasons:

i

9. Power Lesel To which Re>tricted,If Any (Net MWe):
10. Re:nons For Restrictions. lf Any:

This Month Yr..to.Date Cumulatise

11. Hours In Reporting Period 719 2879 90.8$

0 h9,2h7.0 12 Number Of Hours Reactor Was Critical 1223.8

13. Reactor Resene Shutdow n Hours -
14. Hours Generator On.Line 0 891.6 L7.096.f;
15. Unit Resene Shutdown Hours - - -

' 0 1,798,560 93,205,82h

16. Gross Thermal Energy Generated (MWH) .

17 Gross Electrical Energy Generated (MWH) 10** ,_,

558,890 28,786,8h0

18. Net Electrical Energy Generated (MWH) 0 522_los 27_Ols_098 0 37,o 5) , g

, 19. Unit Senice Factor

20. Unit Asailability Factor 0 31.0 51.8
21. Unit Capacity Factor (Using NL)C Net) 0 28.6 h6.9
22. Unit Capacity Factor (Using DER Net) 0  ??.s 97.0
23. Unit Forced Outage Rate 100 69.0 1h.6
24. Shutdowns Scheduled Oser Nest 6 Months (Ty pe. Date.and Duration of Eachl:
25. If Shut Down At End Of Report Period, Estimated Date of Startup: 5-9-82
26. Units in Test Status (Prior to Commercial Operationi: Forecast A chies ed INITI A L CRillCA LITY

, INiil AL ELECTRICITY CO\lMERCI AL OPER ATION -

!

  • Based en Condenser back pressure
  • w0...4 f

ter (0/I7) 8205120222 820507 g

PDR ADOCK 05000255 PDR -

9

AVERAGE DAILY UNIT POWER LEVEL DOCKET NO. 50-255 UNIT Pnl!nndeo DATE 5-7-82 COSIPLETED 13Y DPeterscn TELEPIIONE 616 761-8913 4

510.Nlli April 1982 DAY AVERAGE DAILY POWER LEVEL DAY AVER AGE DAILY POWER LEVEL (51We-Net) (SIWE-Net) 0 1

17 n

, 0 l8 0 .

3 0 19 0 4 0 20 0 3 0 0 21 6 o 0 g

7 0 23 0 8 0 0 24 9 0 o 23, 10 0 26 0 11 0 27 n-g, 0 28 0 f 13 0 29 0 la 0 0 30 0

15 31 16 0 INST RUCTIONS On this liirnut hst the nerJJe daily unit power laelin ilWe. Net for caeh day in the reportine month.Gimpute to n: nearest whole me;2wau.

(9/77)

UNITSilUTDOWNS AND POWER RfDUCT10NS DOCKET NO. 50-255 UNIT NAME W14 ca 4c DATE G-5 A' COMPl.ETED fly NJn -%- no-REPORT MONTil ^rM' icB2 TELEPlf0NE 4' 4 76L_qa,3

= -

= e .3 .o e .

5

, .2 _r E , .5 4 Licensee g% g% Cause & Corrective Ni . . Daic g 3g j jg5 Event %7 9. ~j Auton to 6-

$2 5 3 5i cg Report " EU 5' Present ecurrente e o Q

8 820323 F 719 A 1 82-12 Steara Generator Tube Leakage I 2 3 4 F: Forccd Reason : Method: Exlubit G - Instructions S: Scheduled A liiluipment Failure (Explain) 1 -Manual for Preparation of Data 11-Maintenance of Test 2 Manual Scram. Entiy Sheets for lacensee C Refueling 3 Automatic Scram. Event Report (1.1 RI File (NilRI G.

D Regulatory Restriction 4-Olher (Explain ) 0161)

E-Operator Training & License lixamination F-Ad minist rative 5 G-Operational I i ror (I!xplain) Estubit I - Same Source p8/77) Il-Olher ( E xplain )

0

SU?&JdtY OF OPERATING EXPERIENCE FOR THE MONTH OF APRIL 1982 The Plant was taken off line because of Steam Generator tube leakage in excess of the Technical Specification limit on March 2h. Investigation and repair of the leakage continued through the end of the month of April.

l i

i i

t

, . - ~ -_.. . - _ _ - - _ _ , . _ , , . . . ~_ _ - , _ _ . , . , . _ . ,,_ ..c__ ,_ - - _ _ . _ . _ . .- . _ - - . _ _ , , _ _ - _ _ -. _ _ _ _ _