ML20050L193

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LER 82-003/01T-0:on 820314,unplanned Dilution of RCS Resulted When Operators Were Trying to Restore Shutdown Cooling Flow.Caused by Two Manual Valves Being Partially Open Simultaneously While One Being Opened & Other Closed
ML20050L193
Person / Time
Site: San Onofre Southern California Edison icon.png
Issue date: 03/30/1982
From: Ray H
SOUTHERN CALIFORNIA EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
Shared Package
ML20050L181 List:
References
LER-82-003-01T, LER-82-3-1T, NUDOCS 8204140273
Download: ML20050L193 (1)


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REPORT DATE EVENT DESCAlPTION AND PROB ABLE CONSEQUENCES h a 2 I With the plant in Mode 6, an unplanned dilution of the Reactor Coolant I l o 131 l System occurred while operators were attempting to restore shutdown I lojalI cooling flow. RCS boron concentration remained above Technical I lo lel l Specification limits throughout the event, thus public safety was l IOic_]1 not endangered. I o 7 I I I

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. cAUSE DESCAiPTION AND CORRECTIVE ACTIONS ,

IiIoiI While attempting to restore pump flow, one operator opened the Refuelinct li li l I Water Storace Tank Suction Line Manual valve while another was closina i While the valves were both partia11M A] the RCS Suction Line Manual Valve.

lil3ll open, water was added to the RCS. A caution statement will be added tol 11 121 l the Onerating Procedure for the Shutdown Cooling System. l

) 7 8 9 80 STA US N POWE R OTH E R ST A TUS SCO RY OtsCOVE RY DESCRtPTION NA Operator Observation 11 151 lB l@ l0 l 0 l Ol@l l lAl@l l ACTIVITY CO' TENT RELEASE AVOUNT OF ACTIVITY LOCATION OF RE LE ASE NA NA l l i I 8C9 l I B l @D OF RELE ASElBl@l 3 10 11 44 l l 45 go PE RSONNE L E XPOSUR ES NUUB E R TvPE C E !CairtioN li I:110 I ol o l@l B l@l" N l pes 50sNE t in2u'.5ts No..P E R

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