05000361/LER-1982-154-03, /03L-0:on 821130,following Turbine Trip,Low Pressure Turbine Stop Valve 2UV-2200R Failed to Close.Caused by Excessive Galling Between Disc Stub Shafts & Casing Bore. Clearance Between Shaft & Bore Increased

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/03L-0:on 821130,following Turbine Trip,Low Pressure Turbine Stop Valve 2UV-2200R Failed to Close.Caused by Excessive Galling Between Disc Stub Shafts & Casing Bore. Clearance Between Shaft & Bore Increased
ML20028D303
Person / Time
Site: San Onofre Southern California Edison icon.png
Issue date: 12/29/1982
From: Ray H
SOUTHERN CALIFORNIA EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
Shared Package
ML20028D290 List:
References
LER-82-154-03L, LER-82-154-3L, NUDOCS 8301170303
Download: ML20028D303 (1)


LER-1982-154, /03L-0:on 821130,following Turbine Trip,Low Pressure Turbine Stop Valve 2UV-2200R Failed to Close.Caused by Excessive Galling Between Disc Stub Shafts & Casing Bore. Clearance Between Shaft & Bore Increased
Event date:
Report date:
3611982154R03 - NRC Website

text

NRC FORM 366 U. S. NUCLEAR REGULATORY COMMISSION (7 771 LICENSEE EVENT REPORT CONTROL BLOCK: l l

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8 60 61 DOCKET NUM8ER 68 98 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROB ABLE CONSEQUENCES h 10121 IWith the plant in Mode 1 and followino a turbine trip. low pressure turbine stop valvel l2VV-2200R located on Low Pressure Turbine #2 failed to close fully and was declared o 3 in i4; l inoperable. Since the affected steam lead was isolated by closing the control l

IO l s t Ivalve on the lead, there was no impact on the health and safety of plant personnel g

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(See also LER 82-153).

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