ML20028D303

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LER 82-154/03L-0:on 821130,following Turbine Trip,Low Pressure Turbine Stop Valve 2UV-2200R Failed to Close.Caused by Excessive Galling Between Disc Stub Shafts & Casing Bore. Clearance Between Shaft & Bore Increased
ML20028D303
Person / Time
Site: San Onofre Southern California Edison icon.png
Issue date: 12/29/1982
From: Ray H
SOUTHERN CALIFORNIA EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
Shared Package
ML20028D290 List:
References
LER-82-154-03L, LER-82-154-3L, NUDOCS 8301170303
Download: ML20028D303 (1)


Text

NRC FORM 366 U. S. NUCLEAR REGULATORY COMMISSION (7 771 LICENSEE EVENT REPORT CONTROL BLOCK: l 1

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(PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) lo l1l8 9l c l ALICENSEE 7

l S lCODE 0 l 5 l142 l@l 15 0 l0 l- l 0LICENSEl 010 l 010 l- l0 l 025 l@l4 NUMBER 26 l1 l1 11 LICENSE TYPE l1JOl@S7 CAT l 58 l@

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10111 3vc l60L l@l 0 l 5 DOCKET l0l0 l 0 l 3 l 668 l 198 l@lEVENT 1 l DATE 1 l 3 l 0 l 8 l 2 l@l1 74 75 REPORT DATEl 2 l 219 80 l 8 l 2 l@

7 8 61 NUM8ER EVENT DESCRIPTION AND PROB ABLE CONSEQUENCES h 10121 IWith the plant in Mode 1 and followino a turbine trip. low pressure turbine stop valvel o 3 l2VV-2200R located on Low Pressure Turbine #2 failed to close fully and was declared  ;

in i4; l inoperable. Since the affected steam lead was isolated by closing the control l IO l s t Ivalve on the lead, there was no impact on the health and safety of plant personnel g i O is I lor the public. (See also LER 82-153). l i

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7 8 9 to 11 12 13 18 19 20 SEQUENTI AL OCCURRENCE REPORT REVISION EVENT YEAR REPOR T NO. CODE TYPE N O.

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44 47 JJ 34 36 31 40 43 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h li i o l lThe valve was disassembled during the current outage and inspection revealed i i i l excessive galling between the disc stub shafts and the casing bore. Clearance l

, , lbetween shaf t and bore was increased within drawing tolerances by machining i l

ii 13 l l the stub shaf ts.

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