05000361/LER-1982-162-03, /03L-0:on 821207,w/plant in Mode 1,low Pressure Tubine Stop Valve 2UV-2200V on Low Pressure Turbine 3 Failed to Fully Close.Caused by Excessive Galling Between Disc Stub Shaft & Casing Bore.Stub Shaft Cleaned

From kanterella
(Redirected from ML20028D847)
Jump to navigation Jump to search
/03L-0:on 821207,w/plant in Mode 1,low Pressure Tubine Stop Valve 2UV-2200V on Low Pressure Turbine 3 Failed to Fully Close.Caused by Excessive Galling Between Disc Stub Shaft & Casing Bore.Stub Shaft Cleaned
ML20028D847
Person / Time
Site: San Onofre Southern California Edison icon.png
Issue date: 01/06/1983
From: Ray H
SOUTHERN CALIFORNIA EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
Shared Package
ML20028D846 List:
References
LER-82-162-03L, LER-82-162-3L, NUDOCS 8301200018
Download: ML20028D847 (1)


LER-1982-162, /03L-0:on 821207,w/plant in Mode 1,low Pressure Tubine Stop Valve 2UV-2200V on Low Pressure Turbine 3 Failed to Fully Close.Caused by Excessive Galling Between Disc Stub Shaft & Casing Bore.Stub Shaft Cleaned
Event date:
Report date:
3611982162R03 - NRC Website

text

NRC FOIM 366 U. S. NUCLEAR RE*ULATZY COMMISSION LICENSEE EVENT REPORT CONTROL 8 LOCK: l l

l l

l l lh (PLEASE PRINT 0R TYPE ALL REQUIRED INFORG8ATIONI 1

6 ITI l I c l A l S l O f S l 2l@l010l-l010101010l 1010l@l411Il11Ill@l l

l@

7 8 9 LICENSEE CODE 14 15 LICENSE MunsSER 25 26 LICENSE TYPE JO SFCAT58 CON'T A

SZR% L.LJ@l 015101010131 s li Gli 12 l a l71 a l 2 i@l 01110161813 l@

i 8

60 6t DOCKET NUMBER e

e EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROSA8LE CONSEQUENCES h 1012l lWith the plant in Mode 1, low pressure turbine stop valve 2VV-2200V located on Low I

l Pressure Turbine #3 failed to close fully and was declared inoperable.

Since the l

0 3 laffected steam lead was isolated by closing the control valve on the lead, there l

0 4 lwas no impact on the health and safety of plant personnel or the public. '(See 1

0 s lalso LER's82-153 and 82-154.)

l 0 s 0 7 1 1

I 1010 t I 80 7

89 DE OE S SCO E COMPON ENT CODE SUB ode S

E 17171 IH I A l@ y@ O@ l Vl Al Ll El Xl l@ g@ g @

7 8

9 10 ft 12 13 18 19 20 SEQUENT!AL OCCURRENCE REPORT REVISION EVENT YEAR REPORT NO.

COOE TYPE N O.'

@ =LER; AOl 8121 l- _J l 1161 21 1/l 10131 LL_j

[---j [0_j

,21 22 23 24 26 27 28 29 30 31 32 TAK N ACTC ONP NT E

HOURS S8 i FOR b 8.

S PFL ER MANUFAC URER lB l@lZ l@

[Z _j@

[Zj@

l 01010l 01 [N_J @

lNl@

W@

lXl9I9I9l@

33 34 35 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h Ii IO I l The valve was disassembled and inspection revealed excessive galling between the I

li li I I disc stub shaft and the casing bore. After machining of the stub shaft, cleaning l

l and reassembly, the valve was returned to operable status on December 28, 1982.

I

, 7 i a i l

l' i 4 l

80 7

8 9 ST S

% POWER OTHER STA TUS IS O RY DISCOVERY DESCRIPTION LB.J@ l 01s 10 l@l N/A

_l LB.d@l l

i s ACTIVITY CO TENT AMOUNT OF ACTIVITY LOCATION OF RELEASE RELEASE @D OF RELE ASE[l}@lN/A l

l N/A l

l.2]

1 6 7

8 9 to 11 44 45 80 PERSONNEL EXPOSURES NUV8E R TYPE

DESCRIPTION

l i l il l 010101@LZ_J@l N/A I

2 nRSONN E'L,~,u'R.ES NuYBER DESCRIPf 60%

1010101@l N/A I

i a 7

8 9 11 12 80 8801200 o/9 s

'in@' "fSa'??ON T

[Lj l N/A l

I 9 7

8 9 10 80 PUBUCITY NRC USE ONLY

'h@l N/f"'

  • brir7k l

lllllgg;;;;;lj 2 o

/

68 69 80 3 7

d 9 10 714-492-7700

{

H.R. Ray p u o., g.

NAvr orenreARea