05000361/LER-1982-168-03, /03L-0:on 821212,indicated Position for Shutdown Control Element Assembly 12 Went from 148 Inches to 120 Inches Resulting in Reactor Trip.Caused by Failure of Reed Switch.Switch Replaced.No Further Corrective Action Planned

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/03L-0:on 821212,indicated Position for Shutdown Control Element Assembly 12 Went from 148 Inches to 120 Inches Resulting in Reactor Trip.Caused by Failure of Reed Switch.Switch Replaced.No Further Corrective Action Planned
ML20028F366
Person / Time
Site: San Onofre Southern California Edison icon.png
Issue date: 01/11/1983
From: Ray H
SOUTHERN CALIFORNIA EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
Shared Package
ML20028F363 List:
References
LER-82-168-03L, LER-82-168-3L, NUDOCS 8302010285
Download: ML20028F366 (1)


LER-1982-168, /03L-0:on 821212,indicated Position for Shutdown Control Element Assembly 12 Went from 148 Inches to 120 Inches Resulting in Reactor Trip.Caused by Failure of Reed Switch.Switch Replaced.No Further Corrective Action Planned
Event date:
Report date:
3611982168R03 - NRC Website

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