ML20024E423

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LER 83-066/03L-0:on 830701,during Creacus Surveillance Testing,Train B Declared Inoperable After Emergency Chilled Water Unit E-335 Failed to Start.Caused by Malfunction of Control Circuitry or Power Supply breaker.W/830801 Ltr
ML20024E423
Person / Time
Site: San Onofre Southern California Edison icon.png
Issue date: 08/01/1983
From: Ray H
SOUTHERN CALIFORNIA EDISON CO.
To: Martin J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
References
LER-83-066-03L, LER-83-66-3L, NUDOCS 8308150011
Download: ML20024E423 (4)


Text

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EVENT DESCRIPTION AND PROB ABLE CONSEQUENCES O'o l o l2 l lWith both Units in Mode 5, at 1215 CREACUS Train "B" was declared inoperable l lo la llafter Emergency Chilled Water Unit E-335 failed to start during CREACUS I lo l4 l lsurveillance testing per Procedure 5023-3-3.20. LC0 3.7.5 Action Statement 'a' l

[olsllwas entered. After E-335 started successfully, the surveillance test was com- l j o j 6 l lpleted. CREACUS Train "B" was declared operable at 0559 on 7/2/83 and the Action l lo l7 l l Statement was satisfied. (See Attachment. ) l o el "

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CAUSE DESCRIPTION AND CORRECTIVE ACTIONS 27 lilo ]lThe failure of E-335 was apparenfly due to either a malfunction of its control l Iili l[ circuitry or a mechanical nalfunction in the E-335 Power Supply Breaker l l,l7 l152-3A0602. E-335 started successfully after transferring from the Unit 3 to  ;

l 3 l 3 l lthe Unit 2 power supply. An investigation of the control circuitry and Supply l

t il 4 l l Breaker 152-3A0602 will be conducted. (See Attachment.)  !

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.- es ATTACHMENT TO LER 83-066 SOUTHERN CALIFORNIA EDISON COMPANY SAN ONOFRE NUCLEAR GENERATING STATION UNIT NO. 2, DOCKET NO. 50-361 SUPPLEMENTAL INFORMATION FOR EVENT DESCRIPTION AND PROBABLE l I

CONSEQUENCES There was no impact on public health or safety since CREACUS Train  ;

"A" remained operable throughout this incident. See also Unit 2 LER No.83-049 and Unit 3 LER No.83-043.

SUPPLEMENTAL INFORMATION FOR CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Corrective actions as required will be initiated. At the conclusion of the investigation, an update to this LER will be issued. ,

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RECEIVED

RPC Southern California Edison Company t= i

$AN ONOFRE NUCLE AR GENER ATING C93 Ag~ '

STATION 'i P.O. Bo x 12 8 ,

S AN CLEMENT E, C ALIFCRNI A 92672 i H. 8. R AY b[I E[,]p' "LEN0aE August 1, 1983 4

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l U.S. Nuclear Regulatory Commission Office of Inspection and Enforcement 1

Region V i 1450 Maria Lane, suite 210 Walnut Creek, California 94596-5368

[ Attention: Mr. J.B. Martin, Regional Administrator 1

Dear Sir:

Subject:

Docket Nos. 50-361 and 50-362 30-Day Report .

Licensee Event Report No.83-066 (Docket No. 50-361)

San onofre Nuclear Generating Station, Units 2 and 3 Pursuant to Sections 6.9.1.13.b of Appendix A, Technical

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Specifications to Facility Operating Licenses NPF-10 and NPF-15 for San Onofre Units 2 and 3, respectively, this submittal provides the required 30-day written report and a copy of Licensee Event Report (LER) No.83-066 addressing an occurrence

' involving Limiting Condition for Operation (LCO) 3.7.5

, associated with the Control Room Emergency Air Cleanup System (CREACUS). Since this occurrence involves a shared system t- between Units 2 and 3, in accordance with NUREG-0161, a single

LER for Unit 2 (Docket No. 50-361) is enclosed.
  • i If there are any questions regarding this event, please contact me. "

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Enclosure:

LER No.'83-066 l

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.. ' .:; O Mr. J.B. Martin cc: A.E. Chaffee (USNRC Resident Inspector, Units 2 and 3)

J.P. Stewart (USNRC Resident Inspector, Units 2 and 3)

U.S. Nuclear Regulatory Commission Office of Inspection and Enforcement U.S. Nuclear Regulatory Commission Division of Technical Information and Document Control Institute of Nuclear Power Operations (INPO) 1323u l

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