ML20023B211

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LER 82-152/03L-0:on 821115,during Performance of LIS-RI-01, Differential Pressure Indicating Switch 1E31-N007A Setpoint Found Out of Tolerance in Nonconservative Direction Per Tech Spec 3.3.2.Cause Unknown.Switch Recalibr
ML20023B211
Person / Time
Site: LaSalle Constellation icon.png
Issue date: 12/13/1982
From: Houston R
COMMONWEALTH EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML20023B200 List:
References
LER-82-152-03L, LER-82-152-3L, NUDOCS 8212270148
Download: ML20023B211 (2)


Text

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EVENT DESCRIPTION AND PRC8 ABLE CONSEQUENCES h io i:; l On November 15, 1982 at 0200 hours0.00231 days <br />0.0556 hours <br />3.306878e-4 weeks <br />7.61e-5 months <br />, during the performance of LIS-RI-01, DPIS lE31- g 90 ,3; g N007A setpoint was found out of tolerance in the non-conservative direction per g Technical Specification 3.3.2. DPIS lE31-N007B and lE31-N013B setpoints were found g l o 6 41 i io Isl l within tolerance. These switches would have isolated the Inboard Steam Isolation g Io j6 [ l Valve 1E51-F063 and the Steam Line Warm-up Valve lE51-F076 had an isolation been ,

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I. LER NUMBER: 82-152/03L-0 )

II. LASALLE COUNTY STATION: Unit 1 III. DOCKET NUMBER: 050-373 IV. EVENT DESCRIPTION:

On November 15, 1982 at 0200 hours0.00231 days <br />0.0556 hours <br />3.306878e-4 weeks <br />7.61e-5 months <br />, during the performance of LIS-RI-01, Steam Line High Flow RCIC Isolation Calibration and Functional Test, DPIS lE31-N007A setpoint was found out of tolerance in the non-conserva-tive direction per Technical Specification 3.3.2.

V. PROBABLE CONSEQUENCES OF THE 0':CURRENCE:

At the time of the occurrence the reactor was in the Run mode producing 1575 MWT, 460 MWE. DPIS lE31-N007B and 1E31-N013B setpoints were found within tolerance. These switchas would have isolated the Inboard Steam Isolation Valve IE51-F063 and the Steam Line Warm-Up Valve lE51-F076 had an isolation been required. Safe plant operation was maintained at all times.

VI. CAUSE:

This was an isolated incident. The cause of the setpoint drift is unknown at this time. The Differential Pressure Indicating Switch was manufactured by ITT Barton, Model 288.

VII. CORRECTIVB ACTION:

DPIS lE31-N007A was recalibrated on November 15, 1982 and declared operable.

Prepared by: R. W. Houston