ML19253C978

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LER 79-056/03L-0:on 791108,20 Dysfunctional Fire Barrier Penetrations Found During QA Audit.Caused by Misinterpretation of Tech Specs by Plant Personnel. Inoperable Penetrations Repaired
ML19253C978
Person / Time
Site: Farley Southern Nuclear icon.png
Issue date: 12/07/1979
From: Hairston W
ALABAMA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19253C948 List:
References
LER-79-056-03L, LER-79-56-3L, NUDOCS 7912120459
Download: ML19253C978 (2)


Text

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NRC FORM %6 U.S. NUCLEAR RECUT.ATORY COMMISSION (7-7 74

  • LICENSEE EVENT REPORT CONTROL BLOCK: l l l l l l l (PLEASE PRINT OR TYPE Alt. REQUIRED INFORMATION)

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EVENT OFSCRIPTION AND PROBABLE CONSEQUENCES h o 2 l As ri result of recent NRC and APCo Operations Ouality Assurance Audits. annroximatelv l 10131 l 20 fire barrier penetrations were determined not to be functional or potentially not I lo l4 l l functional on 11/8/79 and 11/9/79. Tech. Spec. 3.7.1.2 reauires all fire barrier 1 o s l pentrations protecting safety related areas to be functional. Tech. Spec. 3.7.1.2 l 0 16 I action statement reautrements were met unon d1<:covery of the oroblem. The health and I l 0 l 7 I L safety of the public were not af fected by this event. I O R l 7 t. 9 80 COI[E CO$e SEs*CO$E COMPON EN T CODE SUS DE $ M

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LER 79-056/03L-0 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS

. This event was caused by improper interpretation by plant personnel of which penetrations and walls fall under Technical Specifications and of procedures regarding fire barrier penetration operability which resulted in failure to initiate LCO action, requirements.

The following corrective actions have been or will be taken:

1. LCO action requirements were met upon discovery of the problem.
2. Action was taken to repair inoperable penetrations.
3. Memoranda have been issued to appropriate plant personnel clari-

- fying procedural and LCO requirements.

4. Action is being initiated to re-inspect all fire walls and associated penetrations. Results of this inspection will be reported in a revision to this LER.

= 1540 009

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