ML061170008

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IR 05000338-06-002, IR 05000339-06-002, IR 07200016-06-001; 01/01/2006 - 03/31/2006; North Anna Units 1 & 2, & North Anna Independent Spent Fuel Storage Installation. Routine Integrated Resident and Regional Inspector Report. Event Follow-u
ML061170008
Person / Time
Site: North Anna  Dominion icon.png
Issue date: 04/26/2006
From: Landis K
NRC/RGN-II/DRP/RPB5
To: Christian D
Virginia Electric & Power Co (VEPCO)
References
IR-06-001, IR-06-002
Download: ML061170008 (44)


See also: IR 07200016/2006001

Text

April 26, 2006

Virginia Electric and Power Company

ATTN.: Mr. David A. Christian

Sr. Vice President and

Chief Nuclear Officer

Innsbrook Technical Center - 2SW

5000 Dominion Boulevard

Glen Allen, VA 23060-6711

SUBJECT: NORTH ANNA POWER STATION - NRC INTEGRATED INSPECTION

REPORT NOS. 05000338/2006002, 05000339/2006002 AND

07200016/2006001

Dear Mr. Christian:

On March 31, 2006, the United States Nuclear Regulatory Commission (NRC) completed an

inspection at your North Anna Power Station, Units 1 and 2, and the North Anna Independent

Spent Fuel Storage Installation. The enclosed integrated inspection report documents the

inspection results, which were discussed on April 11, 2006 with Mr. Jack Davis and other

members of your staff.

The inspections examined activities conducted under your licenses as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your

licenses. The inspectors reviewed selected procedures and records, observed activities, and

interviewed personnel.

Based upon the results of this inspection, one self-revealing finding and one NRC-identified

finding of very low safety significance (Green) were identified. The findings were determined to

involve a violation of NRC requirements. However, because of the very low safety significance

and because they were entered into your corrective action program, the findings are treated as

non-cited violations (NCV) consistent with Section VI.A of the NRC Enforcement Policy. In

addition, one licensee- identified violation, which was determined to be of very low safety

significance, is listed in Section 4OA7 of this report. If you contest any non-cited violation in this

report, you should provide a response within 30 days of the date of this inspection report, with

the basis for your denial, to the United States Nuclear Regulatory Commission, ATTN:

Document Control Desk, Washington, D.C. 20555-0001; with copies to the Regional

Administrator, Region II; the Director, Office of Enforcement, United States Nuclear Regulatory

Commission, Washington, D.C. 20555-0001; and the NRC Resident Inspector at the North

Anna Power Station.

In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter, its

enclosure, and your response, if any, will be available electronically for public inspection in the

NRC Public Document Room or from the Publicly Available Records (PARS) component of

VEPCO 2

NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Kerry D. Landis, Chief

Reactor Projects Branch 5

Division of Reactor Projects

Docket Nos.: 50-338, 50-339,72-016

License Nos.: NPF-4, NPF-7, SNM-2507

Enclosure: Inspection Reports 05000338/2006002, 05000339/2006002, and

07200016/2006-001

cc w/encl: (See page 3)

_________________________

OFFICE RII:DRP RII:DRP RII:DRS RII:DRS RII:DRS RII:DRS RII:DRS

SIGNATURE JTR GJW GWL1 GWL1 for PKV PKV for HJG1

NAME JReece GWilson GLaska GJohnson KVanDoorn BMiller HGepford

DATE 04/21/2006 04/21/2006 04/24/2006 04/24/2006 04/24/2006 04/24/2006 04/24/2006

E-MAIL COPY? YES NO YES NO YES NO YES NO YES NO YES NO YES NO

OFFICE RII:DRS RII:DRS RII:DRS RII:DRS

SIGNATURE RCH for NJG1 PKV for RCH

NAME RHamilton JGriffis RChou RHaag

DATE 04/24/2006 04/24/2006 04/24/2006 04/24/2006

E-MAIL COPY? YES NO YES NO YES NO YES NO YES NO YES NO YES NO

VEPCO 3

cc w/encl:

Chris L. Funderburk, Director

Nuclear Licensing and

Operations Support

Virginia Electric and Power Company

Electronic Mail Distribution

Jack M. Davis

Site Vice President

North Anna Power Station

Electronic Mail Distribution

Executive Vice President

Old Dominion Electric Cooperative

Electronic Mail Distribution

County Administrator

Louisa County

P. O. Box 160

Louisa, VA 23093

Lillian M. Cuoco, Esq.

Senior Counsel

Dominion Resources Services, Inc.

Electronic Mail Distribution

Attorney General

Supreme Court Building

900 East Main Street

Richmond, VA 23219

Distribution w/encl: (See page 4)

VEPCO 4

Letter to David A. Christian from Kerry D. Landis dated April 26, 2006.

SUBJECT: NORTH ANNA POWER STATION - INTEGRATED INSPECTION REPORT

05000338/2006002 AND 05000339/2006002

Distribution w/encl.:

S. Monarque, NRR

L. Slack, RII

RIDSNRRDIPMLIPB

PUBLIC

U. S. NUCLEAR REGULATORY COMMISSION

REGION II

Docket Nos.: 50-338, 50-339,72-016

License Nos.: NPF-4, NPF-7, SNM-2507

Report Nos.: 05000338/2006002, 05000339/2006002, 07200016/2006001

Licensee: Virginia Electric and Power Company (VEPCO)

Facilities: North Anna Power Station, Units 1 & 2

North Anna Independent Spent Fuel Storage Installation

Location: 1022 Haley Drive

Mineral, Virginia 23117

Dates: January 1, 2006 - March 31, 2006

Inspectors: J. Reece, Senior Resident Inspector

G. Wilson, Resident Inspector

K. Van Doorn, Senior Reactor Inspector, Section 1R08

B. Miller, Reactor Inspector, Section 1R08

R. Chou, Reactor Inspector, Section 1R08

G. Laska, Senior Operations Examiner, Section 1R11

G. Johnson, Operations Engineer, Section 1R11

H. Gepford, Health Physicist, Sections 2OS1, 4OA1, and 4OA5

R. Hamilton, Senior Health Physicist, Sections 2PS2 and 4OA1

J. Griffis, Health Physicist, Section 2OS2

L. Garner, Senior Project Engineer, Section 1R13

Approved by: K. Landis, Chief, Reactor Projects Branch 5

Division of Reactor Projects

Enclosure

TABLE OF CONTENTS

SUMMARY OF FINDINGS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 3

REPORT DETAILS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 5

REACTOR SAFETY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 5

1R04 Equipment Alignment . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 5

1R05 Fire Protection . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 5

1R07 Heat Sink Performance . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 6

1R08 Inservice Inspection (ISI) Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 7

1R11 Licensed Operator Requalification Program . . . . . . . . . . . . . . . . . . . . . . . . . . 10

1R12 Maintenance Effectiveness . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 11

1R13 Maintenance Risk Assessments and Emergent Work Evaluation . . . . . . . . . . 12

1R15 Operability Evaluations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 14

1R19 Post Maintenance Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 14

1R20 Refueling and Other Outages . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 15

1R22 Surveillance Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 17

1EP6 Drill Evaluation . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 17

RADIATION SAFETY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 18

2OS1 Access Controls To Radiologically Significant Areas . . . . . . . . . . . . . . . . . . . . 18

2OS2 As Low As Reasonably Achievable (ALARA) Planning and Controls . . . . . . . 20

2PS2 Radioactive Material Processing and Transportation . . . . . . . . . . . . . . . . . . . . 21

OTHER ACTIVITIES . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 22

4OA1 Performance Indicator Verification . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 22

4OA2 Identification and Resolution of Problems . . . . . . . . . . . . . . . . . . . . . . . . . . . . 23

4OA5 Other Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 24

4OA6 Meetings, including Exit . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 27

4OA7 Licensee-Identified Violation . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 27

ATTACHMENT: SUPPLEMENTARY INFORMATION

Key Points of Contact . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-1

List of Items Opened, Closed, and Discussed . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-2

List of Documents Reviewed . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-3

List of Acronyms . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-11

Enclosure

SUMMARY OF FINDINGS

IR 05000338/2006-002, IR 05000339/2006-002, IR07200016/2006-001; 01/01/2006 -

03/31/2006; North Anna Power Station Units 1 & 2, and North Anna Independent Spent Fuel

Storage Installation. Routine Integrated Resident and Regional Inspector Report. Event

Followup.

The report covered a three-month period of inspection by the resident inspectors and

announced inspections by a senior operations examiner, an operations engineer, a senior

health physicist, two health physicists, a senior reactor inspector, and two reactor inspectors

from the region. One self-revealing finding and one NRC-identified finding were identified. The

findings were determined to be non-cited violations (NCV). The significance of most findings is

indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, Significance Determination Process (SDP). Findings for which the SDP does not apply

may be Green or be assigned a severity level after NRC management review. The NRCs

program for overseeing the safe operation of commercial nuclear power reactors is described in

NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.

A. NRC-Identified and Self-Revealing Findings

Cornerstone: Mitigating Systems

Green. An NRC-identified non-cited violation of 10 CFR 50 Appendix B Criterion III was

identified for failure to translate design requirements into procedures. Specifically, the

licensee failed to properly translate the Technical Specification (TS) Operable-

Operability definition into procedures which established the time the environmental

hazard barriers between the turbine building and either the main control room or the

emergency switchgear room were allowed to be inoperable during maintenance. This

issue is documented in the licensees corrective action program as Plant Issues N-

2005-1080 and N-2005-2236.

This issue is more than minor because it could become a more significant condition, in

that the unit could continue to operate at full power with main control room and

emergency switchgear equipment exposed to potentially harsh environmental conditions

(e.g. steam from a high energy line break in the turbine building) for a period of time

greater than that allowed by TS. However, the time period that the pressure boundary

door 2-BLD-STR-S54 was inoperable on March 16, 2005 did not result in a violation of

TS 3.0.3 and thus no performance deficiency existed for that specific event. After

management review, the issue was assigned a significance of Green because the

inoperability period was limited to a maximum of 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> by other TS. (Section 1R13)

Green. A self-revealing non-cited violation of 10 CFR 50, Appendix B, Criterion III was

identified for inadequate design control resulting in a flood potential for the Units 1 and 2

safeguards instrument rack rooms. On July 9, 2005, back flush of control room chiller

service water strainers 2-HV-S-1A and 1B as directed by engineering transmittal ET

N-05-0034, Operability of 2-HV-P-22C, Service Water Pump for 2-HV-E-4C, was

performed in the Unit 2 air conditioning chiller room (ACCR). Following this work

activity, the licensee observed water around a floor drain in the adjacent air conditioning

fan rooms (ACFR) and initiated Plant Issue N-2005-2565 to evaluate the abnormal

Enclosure

condition. Subsequently, the licensee determined that back-flow preventers were not

installed in the floor drains on the ACFRs on both units. The back-flow preventers are

necessary to prevent leakage in the ACCR from bypassing the flood wall protecting the

ACFR and adjoining safeguards instrument rack room from flooding.

The inspectors determined that the finding had a credible impact on safety based on the

potential for flooding to impact the instrument rack room which contains both trains of

Solid State Protection System cabinets used for engineered safeguards. The finding, if

left uncorrected, would result in a more significant safety concern and is consequently

more than minor. A Phase III evaluation was performed for the SDP due to the loss or

degradation of equipment specifically designed to mitigate a flooding event and the

impact on two trains of a safety system. This evaluation concluded that the

performance deficiency was of very low safety significance (Green) based on the

existence of high level alarms for the associated sumps and the response time allowed

for an operator to isolate the leak (approximately 40 minutes). The inspectors also

concluded that this finding had aspects relating to the cross-cutting area of problem

identification and resolution. (Section 4OA5)

B. Licensee-Identified Violation

One violation of very low safety significance was identified by the licensee and has been

reviewed by the inspectors. Corrective actions taken or planned by the licensee have

been entered into the licensees corrective action program. This violation and corrective

action tracking numbers are listed in Section 4OA7 of this report.

Enclosure

REPORT DETAILS

Summary of Plant Status

Unit 1 and Unit 2 began the inspection period at 100 percent power. Units 1 and 2 remained at

or near 100 percent power for the entire reporting period with the following exceptions. Unit 1

experienced a forced outage February 13 - 17, 2006, due to tube leaks in the 6B and 4B

feedwater heaters. Unit 1 entered a refueling outage on March 12, 2006, which continued

throughout the remainder of the inspection period.

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity

1R04 Equipment Alignment

a. Inspection Scope

The inspectors conducted three equipment alignment partial walkdowns to evaluate the

operability of selected redundant trains or backup systems, listed below, with the other

train or system inoperable or out of service. The inspectors reviewed the functional

system descriptions, Updated Final Safety Analysis Report (UFSAR), system operating

procedures, and Technical Specifications (TS) to determine correct system lineups for

the current plant conditions. The inspectors performed walkdowns of selected portions

of the systems to verify that critical components were properly aligned and to identify

any discrepancies which could affect operability of the redundant train or backup

system.

  • Unit 2 train B Low Head Safety Injection (LHSI) equipment during planned

maintenance on the 2-SI-P-1A;

  • Units 1 and 2 Switchyard, during planned maintenance on the #1 and #3

busses; and,

  • Unit 1 train A LHSI, while 1-SI-P-1B was inoperable for motor operated valve

preventative maintenance.

b. Findings

No findings of significance were identified.

1R05 Fire Protection

a. Inspection Scope

The inspectors conducted tours of the eleven areas listed below and important to

reactor safety to verify the licensees implementation of fire protection requirements as

described in Virginia Power Administrative Procedure (VPAP)-2401, Fire Protection

Program.

Enclosure

6

The inspectors evaluated, as appropriate, conditions related to: (1) licensee control of

transient combustibles and ignition sources; (2) the material condition, operational

status, and operational lineup of fire protection systems, equipment, and features; and

(3) the fire barriers used to prevent fire damage or fire propagation. Other documents

reviewed are listed in the Attachment.

  • Normal Switchgear Room Unit 1 (fire zone 5-1 / NSR-1);
  • Emergency Switchgear Room Unit 1 (fire zone 6-1a / ESR-1);
  • Emergency Switchgear Room Unit 2 (fire zone 6-2a / ESR-2);
  • Charging Pump Cubicle 1-1C (fire zone 11 Ca / CPC-1C);

MDAFW-1);

  • Battery Room 1 - I Unit 1 (fire zone 7A-1 / BR1-I);
  • Battery Room 1 - II Unit 1 (fire zone 7B-1 / BR1-II);
  • Battery Room 1 - III Unit 1 (fire zone 7C-1 / BR1-III);
  • Battery Room 1 - IV Unit 1 (fire zone 7D - 1/ BR1-IV); and
  • Containment Unit 1 (fire zone 1-1a / RC-1).

b. Findings

No findings of significance were identified.

1R07 Heat Sink Performance

a. Inspection Scope

The inspectors reviewed inspection records, test results, maintenance work orders, and

other documentation to ensure that heat exchanger (Hx) deficiencies that could mask or

degrade performance were identified and corrected. The test procedures and records

were also reviewed to verify that these were consistent with Generic Letter 89-13

licensee commitments, and Electric Power Research Institute (EPRI) Heat Exchanger

Performance Monitoring Guidelines. The risk significant Hx reviewed was the Unit 1 B

Component Cooling (CC) Heat Exchanger, which was tagged out for inspection and

cleaning. The inspectors reviewed CC Hx inspection and cleaning procedures,

completed work orders, design specification sheets, and tube plugging margins to verify

that test results were consistent with design acceptance criteria, inspection methods and

performance of the Hx under the current maintenance frequency were adequate, and to

verify minimum flow requirements and Hx design bases were being maintained.

Additionally, the inspectors reviewed Plant Issue N-2006-0257, regarding CC Hx B

elevated differential pressure, for potential common cause problems and other issues

which could affect system performance to confirm that the licensee was entering

problems into the corrective action program and initiating appropriate corrective actions.

Enclosure

7

The inspectors reviewed Hx test condition reports regarding foreign material found

during recent and past CC Hx inspections. In addition, the inspectors conducted a walk

down of all four CC Hxs and the related service water piping to assess general material

condition and to identify any degraded conditions.

b. Findings

No findings of significance were identified.

1R08 Inservice Inspection (ISI) Activities

.1 Piping Systems ISI

a. Inspection Scope

On March 13-17, 2006, the inspectors reviewed the implementation of the licensees ISI

program for monitoring degradation of the reactor coolant system boundary and the risk

significant piping system boundaries for Unit 1. The inspectors selected a sample of

American Society of Mechanical Engineers (ASME) Boiler and Pressure Vessel Code,

Section XI required examinations and a sample of risk-informed ISI Program

examinations.

The inspectors conducted an on-site review of nondestructive examination (NDE)

activities to evaluate compliance with TS, ASME Section XI and ASME Section V

requirements, 1995 Edition through 1996 Addenda, and to verify that indications and

defects (if present) were appropriately evaluated and dispositioned in accordance with

the requirements of ASME Section XI, IWB-3000 or IWC-3000 acceptance standards.

Specifically, the inspectors observed the following examinations:

Ultrasonic Testing

Steam Generator Crossover Leg;

  • 16"-WFPD-23-601C-Q2, Weld #16A, Main Feedwater to B Steam

Generator;

  • 6"-WFPD-14-901, Weld #SW-44, Main Feed Line to Bypass Feed Line;

and,

  • 6"-WFPD-15-901, Weld #7, Main Feedwater Bypass Line.

Magnetic Particle

  • 6"-WFPD-14-901, Weld #SW-44, Main Feed Line to Bypass Feed Line;

and,

  • 6"-WFPD-15-901, Weld #7, Main Feedwater Bypass Line.

Enclosure

8

The inspectors reviewed the following examination records in addition to the records for

the above observed examinations:

Ultrasonic Testing

  • 12"-SI-14-153A-Q2, Weld #41A, Low Head Safety Injection suction

piping;

  • 12"-SI-14-153A-Q2, Weld #SW-39, Low Head Safety Injection suction

piping;

  • 12"-SI-14-153A-Q2, Weld #85B, Low Head Safety Injection suction

piping; and,

  • 12"-SI-14-153A-Q2, Weld #26, Low Head Safety Injection suction piping.

Liquid Penetrant

  • 12"-SI-14-153A-Q2, Weld #41A, Low Head Safety Injection suction

piping;

  • 12"-SI-14-153A-Q2, Weld #SW-39, Low Head Safety Injection suction

piping;

  • 12"-SI-14-153A-Q2, Weld #85B, Low Head Safety Injection suction

piping; and,

  • 12"-SI-14-153A-Q2, Weld #26, Low Head Safety Injection suction piping.

Qualification and certification records for examiners, inspection equipment, and

consumables along with the applicable NDE procedures for the above ISI examination

activities were reviewed and compared to requirements stated in ASME Section V and

Section XI.

Pressure boundary welding activities associated with ASME Class 2 components were

reviewed to verify the welding process and examinations were performed in accordance

with the ASME Code Sections III, V, IX, and XI requirements. The inspectors reviewed

weld data sheets, the welding procedure specification, supporting welding procedure

qualification records, welder qualification records, weld rod material certifications, and

preservice examination results for the following welds and subsequent weld repairs:

  • 10"-SI-214-153A-Q2, Weld #90, Low Head Safety Injection piping and its

associated weld repairs; and,

  • 10"-RS-9-153A-Q2, Weld #10, Recirculation Spray piping and its

associated weld repairs.

The inspectors performed a review of piping system related problems that were

identified by the licensee and entered into the corrective action program. The inspectors

reviewed these corrective action documents to confirm that the licensee had

appropriately described the scope of the problems and had implemented effective

corrective actions. Specifically, the inspectors reviewed the licensees augmented

examination activities with respect to through wall leaks found on the LHSI piping during

the operating cycle.

Enclosure

9

b. Findings

No findings of significance were identified.

.2 Boric Acid Corrosion Control ISI

a. Inspection Scope

On March 13-17, 2006, the inspectors reviewed the licensees Boric Acid Corrosion

Control Program (BACCP) to ensure compliance with commitments made in response

to NRC Generic Letter 88-05 Boric Acid Corrosion of Carbon Steel Reactor Pressure

Boundary and Bulletin 2002-01 Reactor Pressure Vessel Head Degradation and

Reactor Coolant Pressure Boundary Integrity.

The inspectors conducted an on-site record review and an independent walk-down of

the reactor building to evaluate compliance with licensee BACCP requirements and 10

CFR Part 50, Appendix B, Criterion XVI, Corrective Action, requirements. In particular,

the inspectors verified that licensee visual examinations focused on locations where

boric acid leaks can cause degradation of safety significant components and that

degraded or non-conforming conditions were properly identified in the licensees

corrective action system.

The inspectors reviewed the licensees program implementation procedures and a

sample of plant issue reports (corrective action documents) to ensure that leaks were

being identified and addressed at an appropriate threshold. A sample review of

engineering evaluations was also completed for boric acid deposits found on reactor

coolant system piping and other ASME Code Class components to verify that the

minimum design code required section thickness had been maintained for any affected

component(s). The inspectors also reviewed the licensees corrective actions

implemented in response to a Green NCV identified during the previous outage on Unit

2. Specifically, the inspectors reviewed corrective actions associated with training on

boric acid identification and reporting and actions associated with the implementation of

boric acid walkdown procedures.

b. Findings

No findings of significance were identified.

.3 Steam Generator Tube ISI

a. Inspection Scope

The inspectors reviewed activities, plans, a pre-outage degradation assessment, and

procedures for the inspection and evaluation of the 1B steam generator Inconel Alloy

690TT tubing, to determine if the activities were being conducted in accordance with TS

and applicable industry standards. Data gathering, analysis, and evaluation activities

were reviewed. The inspectors reviewed data results for tubes R18C16, R16C16,

Enclosure

10

R16C17, R29C51, R24C58, and R03C58 to verify the adequacy of the licensees

primary, secondary, and resolution analyses. The inspectors observed the licensee

perform the video/visual inspection in the lower bowl area of the steam generator to

determine if any foreign materials or debris were present. The inspectors observed the

licensees video probe inspection of the upper tube plate area around the periphery,

down the tube lane under Row 1 U-bends, and in-bundle down selected tube columns.

The inspectors observed the licensees Quality Control examiner oversee the vendor

inspection for foreign objects or debris before the closing of the lower manway in the

steam generator. The inspectors also reviewed data operators and analysts

certifications and qualifications, including medical exams.

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification Program

.1 Biennial Review

a. Inspection Scope

The inspectors reviewed the facility operating history and associated documents in

preparation for this inspection. During the week of January 23, 2006, the inspectors

reviewed documentation, interviewed licensee personnel, and observed the

administration of simulator operating tests associated with the licensees operator

requalification program. Each of the activities performed by the inspectors was done to

assess the effectiveness of the licensee in implementing requalification requirements

identified in 10 CFR 55, Operators Licenses. The evaluations were also performed to

determine if the licensee effectively implemented operator requalification guidelines

established in NUREG-1021, Operator Licensing Examination Standards for Power

Reactors, and Inspection Procedure 71111.11, Licensed Operator Requalification

Program. The inspectors also reviewed and evaluated the licensees simulation facility

for adequacy for use in operator licensing examinations. The inspectors observed two

operator crews during the performance of the operating tests. Documentation reviewed

included written examinations, Job Performance Measures (JPMs), simulator scenarios,

licensee procedures, on-shift records, simulator modification request records and

performance test records, the feedback process, licensed operator qualification records,

remediation plans, watch standing, and medical records. The records were inspected

against the criteria listed in Inspection Procedure 71111.11. Documents reviewed

during the inspection are listed in the Attachment.

b. Findings

No findings of significance were identified.

Enclosure

11

.2 Requalifications Activities Review

a. Inspection Scope

The inspectors observed an annual licensed operator requalification simulator

examination on March 7, 2006. The scenerio, Simulator Examination Guide SXG-79,

involved a loss of first stage pressure, a loss of the main feedwater pump, a reactor

coolant pump seal failure, and a faulted steam generator.

The inspectors observed crew performance in terms of communications; ability to take

timely and proper actions; prioritizing, interpreting, and verifying alarms; correct use and

implementation of procedures, including the alarm response procedures; timely control

board operation and manipulation, including high-risk operator actions; and oversight

and direction provided by the shift supervisor, including the ability to identify and

implement appropriate TS actions. The inspectors observed the post training critique to

determine that weaknesses or improvement areas revealed by the training were

captured by the instructors and reviewed with the operators.

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness

a. Inspection Scope

For the two equipment issues listed below, the inspectors evaluated the licensees

effectiveness of the corresponding preventive and corrective maintenance. The

inspectors performed walkdowns of the accessible portions of the systems, performed

reviews of procedures and evaluations, and held discussions with system engineers.

The inspectors compared the licensees actions with the requirements of the

Maintenance Rule (10 CFR 50.65) using VPAP-0815, Maintenance Rule Program, and

Engineering Transmittal CEP-97-0018, North Anna Maintenance Rule Scoping and

Performance Criteria Matrix. Other documents reviewed are listed in Attachment.

  • Elevated internal resistance readings obtained for the 1J Emergency Diesel

Generator indicating potential for damaged cells while performing Work Order

(WO) 726061-01; and,

  • The maintenance rule criteria for 0-AAC-DG-0M, Station Blackout Generator,

was exceeded, Plant Issue N-2006-0357.

b. Findings

No findings of significance were identified.

Enclosure

12

1R13 Maintenance Risk Assessments and Emergent Work Evaluation

a. Inspection Scope

The inspectors evaluated, as appropriate, for the four plant situations listed below: (1)

the effectiveness of the risk assessments performed before maintenance activities were

conducted; (2) the management of risk; (3) that, upon identification of an unforseen

situation, necessary steps were taken to plan and control the resulting emergent work

activities; and (4) that maintenance risk assessments and emergent work problems

were adequately identified and resolved. The inspectors verified that the licensee was

complying with the requirements of 10 CFR 50.65 (a)(4) and the data output from the

licensees safety monitor associated with the risk profile of Units 1 and 2. Other

documents reviewed are listed in Attachment.

  • Unit 1 downpower with 1-CC-E-1B, 0-AAC-DG-0M, 1-PT-230.3, 1-PT-33.7

series, rack work and C Reserve Station Service Transformer (RSST) on

overhead lines on January 25, 2006;

  • 1-HV-E-4B, 1-IA-C-1, 1-PT-14.2, 1-PT-213.2B.1, 1-PT-213.35B, rack work,

switchyard work and C RSST on overhead lines on February 16, 2006;

  • Emergent work on the Alternate AC Diesel Generator with planned work on

instrument racks, switchyard, and C RSST energized on overhead lines on

March 3, 2006; and,

  • Emergent work on 2-CC-TV-204B with planned work on instrument racks,

switchyard, 1-PT-83.12H and C RSST energized on overhead lines on March

14, 2006.

In addition, the inspectors completed an in-office review of WO 00494074-06, repair of

control room pressure barrier door 2-BLD-STR-S54-11.

b. Findings

Introduction: A Green, NRC-identified non-cited violation (NCV), involving the Mitigating

Systems Cornerstone, was identified for failure to translate design requirements into

procedures as required by 10 CFR 50 Appendix B Criterion III. Specifically, the licensee

failed to properly translate the TS Operable-Operability definition into procedures which

established the time the environmental hazard barriers between the turbine building and

either the main control room or the emergency switchgear room were allowed to be

inoperable during maintenance.

Description: On March 16, 2005, the inspectors observed that the licensee considered

themselves in a 24-hour limiting condition for operation while performing WO 00494074-

06 on control room pressure barrier door 2-BLD-STR-S54-11. Since the door functions

as a pressure barrier and also separates the harsh environment designated turbine

building area from the mild environment of the control building, this was inconsistent

with the guidance the NRC had issued in Regulatory Issue Summary (RIS) 2001-009,

Control of Hazard Barriers. The licensee initiated Plant Issue 2005-1080 to address the

concern and Plant Issue 2005-2236 to address subsequent ones identified during the

Enclosure

13

resolution of the former plant issue. The licensee determined that due to a

misapplication of the TS Operable-Operability definition regarding environmental hazard

barriers, they had failed to consider that the supported systems and components should

be considered inoperable when environmental hazard barriers become inoperable. This

problem also extended to certain hazard barriers, including flood barriers, at North Anna

and at its sister plant, the Surry Power Station.

Correct application of the definition on March 16, 2005 would have resulted in entry into

TS 3.0.3, which requires either the TS to be exited or a unit to be in Mode 3 within 8

hours. Door 2-BLD-STR-S54-11 was inoperable for 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> and 52 minutes. Thus, no

TS time limits were exceeded.

Until a long term resolution is developed and implemented, the licensee has established

compensatory measures including appropriately specifying entry into TS 3.0.3 when

required and building temporary hazard barriers for planned evolutions.

Analysis: Not establishing TS required limiting conditions for operations into procedures

is a performance deficiency. This issue is more than minor because it could become a

more significant condition, in that the unit could continue to operate at full power with

main control room and emergency switchgear equipment exposed to potentially harsh

environmental conditions (e.g. steam from a high energy line break in the turbine

building) for a period of time greater than that allowed by TS. However, the time period

that the pressure boundary door 2-BLD-STR-S54-11 was inoperable on March 16, 2005

did not result in a violation of TS 3.0.3 and thus no performance deficiency existed for

that specific event. After management review, the issue was assigned a significance of

Green because the inoperability period was limited to a maximum of 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> by other

TS. Hazard barriers are associated with protecting equipment which mitigate accidents

and thus are associated with the Mitigating Systems Cornerstone.

Enforcement: 10 CFR 50 Appendix B Criterion, Design Basis, requires that design

bases be translated into instructions. Contrary to this, on March 16, 2005, design basis,

i.e., TS definition of Operable-Operability, was not translated into instructions such that

unit operation above Mode 3 would be limited to 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> when environment hazard

barriers were inoperable. Because this finding is of very low safety significance (Green)

and is in the licensees corrective action program as Plant Issues N-2005-1080 and N-

2005-2236, it is being treated as an NCV, consistent with Section VI.A of the NRC's

Enforcement Policy: NCV 05000338, 339/2006002-01, Failure to translate TS operable-

operability definition regarding hazard barriers into instructions as required by 10 CFR

50 Appendix B Criterion III.

1R15 Operability Evaluations

a. Inspection Scope

The inspectors reviewed five operability evaluations affecting risk-significant mitigating

systems, listed below, to assess, as appropriate: (1) the technical adequacy of the

evaluations; (2) whether continued system operability was warranted; (3) whether other

Enclosure

14

existing degraded conditions were considered as compensating measures; (4) whether

the compensatory measures, if involved, were in place, would work as intended, and

were appropriately controlled; (5) where continued operability was considered

unjustified, the impact on TS Limiting Conditions for Operation and the risk significance

in accordance with the SDP. The inspectors review included a verification that the

operability determinations were made as specified by Procedure VPAP-1408, System

Operability.

  • Plant Issue N-2006-0504, during the performance of procedure 0-PT-77.14B for

in-place testing of the Emergency Core Cooling System Pump Room Exhaust Air

Clean-up System (PREACS) Train B filter, the as found leakage for Unit 2

Safeguards Exhaust bypass dampers were out of spec high with Unit 2

Safeguards Exhaust aligned to the Charcoal Filters;

  • Plant Issue N-2006-0520, during the disassembly/inspection of 1-EG-278 check

valve, it was discovered that the in-body seating area of the valve was too wide

and a proper blue check could not be obtained so the valve was declared

operable but degraded;

  • Plant Issue N-2006-1175, containment breach via open containment penetration

coolers inside containment and open component cooling drain valves outside

containment;

  • Plant Issue N-2006-1387, water found in safety-related conduits for

1-FW-P-3A-MOTOR, 1-SI-P-1A-MOTOR, and 1-RS-P-2A-Motor; and,

  • Plant Issue N-2006-1701, for breaker 01-EE-BKR-K/J1-2, the as-found

instantaneous overload setpoints were outside acceptance criteria of Procedure

0-EPM-0302-2.

b. Findings

No findings of significance were identified.

1R19 Post Maintenance Testing

a. Inspection Scope

The inspectors reviewed six post maintenance test procedures and/or test activities, as

appropriate, for selected risk-significant mitigating systems to assess whether: (1) the

effect of testing on the plant had been adequately addressed by control room and/or

engineering personnel; (2) testing was adequate for the maintenance performed; (3)

acceptance criteria were clear and adequately demonstrated operational readiness

consistent with design and licensing basis documents; (4) test instrumentation had

current calibrations, range, and accuracy consistent with the application; (5) tests were

performed as written with applicable prerequisites satisfied; (6) jumpers installed or

leads lifted were properly controlled; (7) test equipment was removed following testing;

and (8) equipment was returned to the status required to perform its safety function.

The inspectors verified that these activities were performed in accordance with licensee

procedure VPAP-2003, Post Maintenance Testing Program.

Enclosure

15

  • Procedure 0-MCM-0803-01, Periodic Disassembly, Inspection, and Repair of

the Control Room Chiller Condenser (1/2-HV-E-4A, B) and the Front Office

Chiller Condenser (1-HV-3A, B, and C), Revision 18, per WO 526179-01 for

2-HV-E-4B;

  • Procedure 0-MCM-0103-04, Disassembly, Inspection and Repair of

Westinghouse/Nuttall Type SU High Speed Gear Drives (Charging Pump Speed

Increase), Revision 13, and Procedure 0-MCM-0103-01, Repair of the

Charging and High Head Safety Injection Pump, Revision 37, per WO 443561;

  • Furmanite leak seal injection of the leaking hinge pin of 2-FW-134, per WO 727585-04;
  • Procedure 0-MPM-0102-02, Motor Driven Auxiliary Feed Pumps Preventive

Maintenance, Revision 1, per WO 720465 for the 1-FW-P-3B lube oil cooler

cleaning;

  • Procedure 1-PT-30.4.2, NIS Source Range channel 11 (N-32) Calibration,

Revision 5, and 1-ICP-NI-32, MS Source Range Channel 11 (N-32) Calibration,

Revision 0, per WO 730503; and,

per WOs 734272, 734273, and 726222.

b. Findings

No findings of significance were identified.

1R20 Refueling and Other Outages

.1 Unit 1 Unscheduled Outage

a. Inspection Scope

Unit 1 began an unscheduled outage on February 13, 2006, due to tube leaks in the 6B

and 4B feedwater heaters. The unit cooled down to Mode 4 (approximately 330

degrees F reactor coolant system (RCS) temperature) in order to secure main

condenser vacuum for repairs to 6B feedwater heater. During the forced outage, the

inspectors evaluated the licensees outage activities to verify that appropriate risk

consideration was given in developing schedules and that the licensee adhered to

administrative risk reduction methodologies. The inspectors also monitored the

licensees risk management of off-normal plant conditions and ensured mitigation

strategies were developed for any loss of key safety functions. The unit was

synchronized to the grid on February 17, 2006, and 98% power was obtained on

February 21, 2006. The licensee subsequently performed a coast down in preparation

for a refueling outage.

b. Findings

No findings of significance were identified.

Enclosure

16

.2 Unit 1 Refueling Outage

a. Inspection Scope

The inspectors performed the inspection activities described below for the Unit 1

refueling outage that began on March 12, 2006 and ended April 10, 2006. The

inspectors used inspection procedure 71111.20, Refueling and Outage Activities, to

observe portions of the shutdown, cooldown, refueling, maintenance activities, and

startup activities to verify that the licensee maintained defense-in-depth commensurate

with the outage risk plan and applicable TS.

The inspectors monitored licensee controls over the outage activities listed below.

Documents reviewed during the inspection are listed in the Attachment.

  • Licensee configuration management, including daily outage reports, to evaluate

defense-in-depth commensurate with the outage safety plan and compliance

with the applicable TS when taking equipment out of service;

  • Installation and configuration of reactor coolant instruments to provide accurate

indication and an accounting for instrument error;

  • Controls over the status and configuration of electrical systems and switchyard to

ensure that TS and outage safety plan requirements were met;

  • Licensee implementation of clearance activities to ensure equipment was

appropriately configured to safely support the work or testing;

generators, when relied upon, were a viable means of backup cooling;

  • Controls to ensure that outage work was not impacting the ability to operate the

spent fuel pool cooling system during and after-core offload;

alternative means for inventory addition, and controls to prevent inventory loss;

  • Reactivity controls to verify compliance with TS and that activities which could

affect reactivity were reviewed for proper control within the outage risk plan;

  • Refueling activities for compliance with TS, to verify proper tracking of fuel

assemblies from the spent fuel pool to the core, and to verify foreign material

exclusion was maintained; and,

  • While the unit did not enter reduced inventory or mid-loop conditions, procedures

were reviewed for commitments to Generic Letter 88-17 to verify that these

commitments were in place, and distractions from unexpected conditions or

emergent work did not affect operator ability to maintain the required reactor

vessel level.

b. Findings

No findings of significance were identified.

Enclosure

17

1R22 Surveillance Testing

a. Inspection Scope

For the six surveillance tests listed below, the inspectors examined the test procedure,

witnessed testing, and reviewed test records and data packages, to determine whether

the scope of testing adequately demonstrated that the affected equipment was

functional and operable and that the surveillance requirements of the TS were met.

In-Service Tests:

  • 2-PT-57.1A, Emergency Core Cooling Subsystem Low Head Safety Injection

Pump (2-SI-P-1A), Revision 48

  • 1-PT-64.4A.2, Casing Cooling Pump (1-RS-P-3A) Biennial Test First

Comprehensive Pump Test, Revision 0

Other Surveillance Tests:

  • 2-PT-82.2, 2J Diesel Generator Test, Simulated Loss of Offsite Power,

Revision 56

Valve Test, Revision 29

(RCP) Bus 2A Undervoltage Test, Revision 9

b. Findings

No findings of significance were identified.

Cornerstone: Emergency Preparedness

1EP6 Drill Evaluation

a. Inspection Scope

On February 21, 2006, the inspectors reviewed and observed the performance of an

Emergency Planning Drill that involved a simulation of an earthquake, major break Loss

of Coolant Accident (LOCA), and equipment malfunctions, resulting in a site area

emergency and subsequent general emergency. The inspectors assessed emergency

procedure usage, emergency plan classification, notifications, and the licensees

identification and entrance of any drill problems into their corrective action program.

This inspection evaluated the adequacy of the licensees conduct of the drill and critique

performance. Drill issues were captured by the licensee in their corrective action

program and were reviewed by the inspectors.

Enclosure

18

b. Findings

No findings of significance were identified.

2. RADIATION SAFETY

Cornerstone: Occupational Radiation Safety

2OS1 Access Controls To Radiologically Significant Areas

a. Inspection Scope

Access Controls. The inspectors reviewed and evaluated licensee guidance and its

implementation for controlling and monitoring worker access to radiologically significant

areas and tasks associated with the 2006 Unit 1 Refueling Outage (RFO). The

inspectors evaluated changes to, and adequacy of, procedural guidance; directly

observed implementation of established administrative and physical radiological

controls; appraised radiation worker and technician knowledge of, and proficiency in

implementing, radiation protection activities; and assessed radiation worker exposures

to radiation and radioactive material.

The inspectors directly observed controls established for radiation workers and Health

Physics Technician (HPT) staff in potential airborne radioactivity area, radiation area,

high radiation area (HRA), locked high radiation area (LHRA), and very high radiation

area (VHRA) locations. Controls and their implementation for LHRA, LHRA > 15 rem/hr,

and VHRA keys, and for storage of irradiated material within the spent fuel pool were

reviewed and discussed in detail. Established radiological controls were evaluated for

selected RFO tasks including transfer canal blind flange removal, upper internals set,

head set, refueling operations, valve maintenance, radioactive waste (radwaste)

processing and storage, and radioactive material/waste shipping activities. In addition,

licensee controls for areas where dose rates could change significantly as a result of

plant shutdown and refueling operations were reviewed and discussed.

For selected tasks, the inspectors reviewed Radiation Work Permit (RWP) details and

attended pre-job briefings to assess communication of radiological control requirements

to workers. Occupational worker adherence to selected RWPs and HPT proficiency in

providing job coverage were evaluated through direct observations, remote

observations, and interviews with licensee staff. Electronic dosimeter (ED) alarm

set-points and worker stay times were evaluated against applicable radiation survey

results. Worker exposure as measured by ED and by licensee evaluations of internal

doses during current refueling outage activities were reviewed and assessed

independently. For HRA tasks involving significant dose gradients, e.g., radiological

surveys of the steam generator (S/G) bowl and reactor cavity entry, the inspectors

evaluated the use and placement of whole body and extremity dosimetry to monitor

worker exposure.

Enclosure

19

Postings and physical controls established within the radiologically controlled area

(RCA) for access to the Unit 1 reactor containment building (RCB), the Unit 1 and Unit 2

reactor auxiliary building (RAB) locations, radioactive material storage locations,

decontamination building, and Independent Spent Fuel Storage Installation (ISFSI) were

evaluated during facility tours. The inspectors independently measured radiation dose

rates or directly observed conduct of licensee radiation surveys and results for the

transfer canal, Unit 1 B S/G bowl, reactor cavity, Unit 1 primary filter, posted LHRAs

within the Unit 1 RCB, and select dose significant areas in the RAB. Results were

compared to current licensee surveys and assessed against established postings and

radiation controls. Licensee controls were observed for selected Unit 1 and Unit 2 RAB

LHRA and VHRA locations.

The inspectors evaluated implementation and effectiveness of licensee controls for both

airborne and external radiation exposure. The inspectors reviewed and discussed

selected whole body count analyses conducted between September 2005 and March

2006 to evaluate implementation and effectiveness of personnel monitoring. The

inspectors directly observed processes used for externally contaminated individuals,

including those with potential uptakes of radioactive material. The inspectors reviewed

administrative and physical controls including air sampling, barrier integrity, engineering

controls, and postings for tasks having the potential for individual worker internal

exposures to exceed 30 millirem committed effective dose equivalent.

Radiation protection activities were evaluated against UFSAR, TS, and 10 CFR Parts 19

and 20 requirements. Specific assessment criteria included UFSAR Section 12,

Radiation Protection, TS Section 5.4.1, Procedures, and Section 5.7, High Radiation

Area. Detailed procedural guidance and records reviewed for this inspection area are

listed in Sections 2OS1 and 4OA5 of the Attachment.

Problem Identification and Resolution. An audit, a self-assessment, and licensee

Corrective Action Program (CAP) documents associated with access controls to

radiologically significant areas were reviewed and assessed. The inspectors evaluated

the licensees ability to identify, characterize, prioritize, and resolve the identified issues

in accordance with VPAP-1501, Deviations, Revision 17 and VPAP-1601, Corrective

Action, Revision 21. Licensee CAP documents associated with access control issues,

personnel radiation monitoring, and personnel exposure events which were reviewed

and evaluated in detail during inspection of this program area are identified in Sections

2OS1, 4OA1, and 4OA5 of the Attachment.

The inspectors completed the 21 specified line-item samples detailed in Inspection

Procedure 71121.01.

b. Findings

No findings of significance were identified.

Enclosure

20

2OS2 As Low As Reasonably Achievable (ALARA) Planning and Controls

a. Inspection Scope

Implementation of the licensee's ALARA program during the 2006 Unit 1 RFO was

observed and evaluated by the inspectors. The inspectors reviewed ALARA planning,

dose estimates, and prescribed ALARA controls for outage work tasks expected to incur

the maximum collective exposures. Reviewed activities included containment

scaffolding, head disassembly, manual valve maintenance, air operated valve

maintenance, and routine HP coverage. Incorporation of planning, established work

controls, expected dose rates, and dose expenditure into the ALARA pre-job briefings

and RWPs for those activities were also reviewed. Work in progress reviews were

inspected for three RWPs in which the actual dose was approaching the estimated dose

for the job. Selected elements of the licensee's source term reduction and control

program were examined to evaluate the effectiveness of the program in supporting

implementation of the ALARA program goals. Shutdown chemistry program

implementation and the resultant effect on RCB and RAB dose rate trending data were

reviewed and discussed with cognizant licensee representatives. Small areas with

abnormally high dose rates forming in the steam generator channel heads were

discussed with HP and Chemistry Supervision.

Trends in individual and collective personnel exposures at the facility were reviewed.

The inspectors examined the dose records of all declared pregnant workers during 2005

and first quarter of 2006 to evaluate total or current gestation doses. Applicable

procedures were reviewed to assess licensee controls for declared pregnant workers.

Trends in the plants three-year rolling average collective exposure history, outage,

non-outage, and total annual doses for selected years were reviewed and discussed

with licensee representatives.

The licensee's ALARA program implementation and practices were evaluated for

consistency with UFSAR Chapter 12, Radiation Protection; 10 CFR Part 20

requirements; Regulatory Guide 8.29, Instruction Concerning Risks from Occupational

Radiation Exposure, February 1996; and licensee procedures. Documents reviewed

during the inspection of this program area are listed in Section 2OS2 of the Attachment.

Problem Identification and Resolution. The inspectors reviewed the CAP documents

listed in Section 2OS2 of the report Attachment that were related to the licensees

ALARA program. The inspectors assessed the licensees ability to identify,

characterize, prioritize, and resolve the identified issues in accordance with VPAP-1501,

Deviations, Revision 17 and VPAP-1601, Corrective Action, Revision 21.

The inspectors completed 22 of the specified line-item samples detailed in Inspection

Procedure 71121.02.

b. Findings

No findings of significance were identified.

Enclosure

21

Cornerstone: Public Radiation Safety

2PS2 Radioactive Material Processing and Transportation

a. Inspection Scope

Waste Processing and Characterization. During system walk-downs, the inspectors

observed selected liquid and solid radwaste processing system components for material

condition and system configuration agreement with the UFSAR and Process Control

Program (PCP). Inspected equipment included the high level and low level waste drain

tanks, waste evaporator tank, evaporator test tanks, spent resin hold-up and dewatering

tanks, and associated piping, valves, and pumps. The inspectors discussed component

function, processing system changes, and radwaste program implementation with

licensee staff.

The 2004 Effluent Report and radionuclide characterizations for each major waste

stream were reviewed and discussed with the radwaste staff. For Unit 2 Dry Active

Waste and liquid waste treatment resin, the inspectors evaluated analyses for

hard-to-detect nuclides, reviewed the use of scaling factors, and examined comparison

results between licensee waste stream characterizations and outside laboratory data.

The licensees waste stream mixing and concentration averaging methodology was

evaluated and discussed with radwaste personnel. The inspectors also discussed the

licensees guidance for monitoring changes in waste stream isotopic mixtures with

knowledgeable personnel.

Radwaste processing activities were reviewed for compliance with the licensees PCP

and UFSAR, Chapter 11. Waste stream characterization analyses were reviewed

against regulations detailed in 10 CFR Part 20, 10 CFR Part 61, and guidance provided

in the Branch Technical Position on Waste Classification and Waste Form. Reviewed

documents are listed in Section 2PS2 of the Attachment.

Transportation. The inspectors directly observed preparation activities for the shipment

of pressurizer safety relief valves. The inspectors noted appropriateness of package

markings and placarding and interviewed shipping technicians regarding Department of

Transportation (DOT) regulations. The inspectors observed radiation surveys of the

transport vehicle prior to shipment.

Six shipping records were reviewed for consistency with licensee procedures and

compliance with NRC and DOT regulations. The inspectors reviewed emergency

response information, DOT shipping package classification, radiation survey results, and

evaluated whether receiving licensees were authorized to accept radioactive materials.

Licensee procedures for opening and closing Type B shipping casks were compared to

recommended vendor protocols and Certificate of Compliance requirements. In

addition, training records for selected individuals currently qualified to prepare

radioactive material shipments were reviewed.

Enclosure

22

Transportation program implementation was reviewed against regulations detailed in

10 CFR Part 20, 10 CFR Part 71, 49 CFR Parts 172-178, and the guidance provided in

NUREG-1608. Training activities were assessed against 49 CFR Part 172 Subpart H.

Documents reviewed during the inspection are listed in Section 2PS2 of the Attachment.

Problem Identification and Resolution. Two audits and licensee CAP documents were

reviewed and assessed. The inspectors evaluated the licensees ability to characterize,

prioritize, and resolve the identified issues in accordance with procedures VPAP-1501,

Deviations, Revision 17 and VPAP-1601, Corrective Action, Revision 21. Documents

reviewed for problem identification and resolution are listed in Section 2PS2 of the

Attachment.

The inspectors completed the six specified line-item samples detailed in Inspection

Procedure 71122.02.

b. Findings

No findings of significance were identified.

4. OTHER ACTIVITIES

4OA1 Performance Indicator Verification

a. Inspection Scope

Cornerstones: Initiating Events and Barrier Integrity

The inspectors sampled licensee submittals for the three Performance Indicators listed

below for U1 and U2. The inspectors reviewed data from the licensees corrective action

program, maintenance rule records, operating logs and maintenance work orders for the

period covering the first quarter 2005 through the fourth quarter 2005. Discussions with

licensee personnel were held by the inspectors regarding the data reviewed. The data

was compared with that displayed on the NRCs public web site. The performance

indicator method of assessment was compared with the guidelines contained in Nuclear

Energy Institute NEI 99-02, "Regulatory Assessment Indicator Guideline," Revision 3,

and the Performance Indicator Frequently Asked Questions (FAQ) list.

  • Scrams with Loss of Normal Hear Removal; and,

Cornerstone: Public Radiation Safety

The inspectors reviewed the Radiological Control Effluent Release Occurrences

Performance Indicator results for the period of January 2005 through December 2005.

For the assessment period, the inspectors reviewed cumulative and projected doses to

the public. The inspectors also reviewed licensee procedural guidance for collecting

Enclosure

23

and documenting Performance Indicator data. Documents reviewed are listed in

Section 4OA1 of the Attachment.

Cornerstone: Occupational Radiation Safety

The inspectors reviewed the Occupational Exposure Control Effectiveness Performance

Indicator results from July 2005 through March 2006. For the assessment period, the

inspectors reviewed documented electronic dosimeter alarms and CAP documents

related to controls for exposure significant areas. The inspectors also reviewed licensee

procedural guidance for collecting and documenting Performance Indicator data.

Report Section 2OS1 contains additional details regarding the inspection of controls for

exposure significant areas. Documents reviewed are listed in Sections 2OS1 and 4OA1

of the Attachment.

During plant tours the inspectors also periodically assessed the Occupational Exposure

Control Effectiveness and the RETS/ODCM Radiological Effluent Occurrence

Performance Indicators by determining if high radiation areas (>1R/hr) were properly

secured and looking for unmonitored radiation release pathways.

b. Findings

No findings of significance were identified. The performance indicators all remained in

the licensee response band (Green).

4OA2 Identification and Resolution of Problems

.1 Daily Review

As required by Inspection Procedure 71152, Identification and Resolution of Problems,

and in order to help identify repetitive equipment failures or specific human performance

issues for follow-up, the inspectors performed a daily screening of items entered into the

licensees corrective action program. This review was accomplished by reviewing daily

Plant Issues summary reports and periodically attending daily Plant Issue Review Team

meetings.

.2 Annual Sample Review

a. Inspection Scope

The inspectors reviewed the licensees assessments and corrective actions for Plant

Issue N-2005-3462, 2H emergency diesel generator developed a coolant leak on the

control side between the #1 and #3 cylinders, during performance of 2-PT-82H. EDG

was manually unloaded and shutdown prior to completion of PT. The Plant Issue was

reviewed to ensure that the full extent of the issue was identified, an appropriate

evaluation was performed, and appropriate corrective actions were specified and

prioritized. The inspectors also evaluated the Plant Issue against the requirements of

Enclosure

24

the licensees corrective action program as specified in VPAP-1601, Corrective Action

Program, VPAP-1501, Deviations, and 10 CFR 50, Appendix B.

b. Findings and Observations

There were no findings of significance identified. On September 6, 2005, the licensee

initiated Plant Issue N-2005-3462 in response to coolant leaks on the Unit 2H

Emergency Diesel Generator (EDG) identified during the monthly surveillance test. The

licensee subsequently completed a functional evaluation and declared a Generic Letter 91-18 condition (operable but degraded) for the component. The inspectors verified the

licensees functional evaluation which considered that the leakrate of the emergency

diesel generator was within the tanks makeup capability and makeup could be

completed without any extraordinary efforts. The inspectors reviewed the history of

coolant leaks for the EDGs which included Plant Issue N-2005-0101 and work order 526277-01, for coolant leaks on the Unit 1H EDG, which was completed on January 9,

2005. During that time, the licensee identified that the water by-pass fitting gaskets that

were manufactured by Cogemica should be replaced with the new model 3000 gaskets

that were manufactured by Garlock. The licensee subsequently scheduled the

replacement of the Unit 1 EDGs gaskets during the 2005 diesel inspections and Unit 2

EDGs gaskets during the 2006 diesel inspections. During the fall of 2005, the

licensees 2H and 2J EDGs incurred failures of their water by-pass fitting gaskets (Plant

Issue N-2005-3462/3633), which resulted in more coolant leaks. The licensee

appropriately determined to review their previous corrective actions and concluded that

their corrective actions were untimely; the inspectors agreed with their conclusion. The

replacement of the by-pass gaskets on the Unit 2 EDGs was subsequently rescheduled

to September 2005 to correct the failed gaskets. The inspectors used IMC 0612 to

review the licensees actions and determined that because the failure of the water

by-pass fitting gaskets did not render the EDGs inoperable, the licenses untimely

corrective action for a condition adverse to quality would be considered a minor violation

of 10 CFR 50, Appendix B Criterion XVI.

4OA5 Other Activities

.1 Independent Spent Fuel Storage Installation (ISFSI) Radiological Controls

a. Inspection Scope

The inspectors conducted independent gamma and neutron surveys of the ISFSI facility

and compared the results to previous surveys. The inspectors also observed and

evaluated implementation of radiological controls, including RWPs and postings, and

discussed the controls with an HPT and HP supervisory staff. Radiological controls for

loading the ISFSI casks were also reviewed and discussed. The inspectors reviewed

environmental thermoluminescent dosimeter records and discussed the use of the

dosimeters and resultant neutron/gamma data with cognizant HP supervisory staff.

Radiological control activities for ISFSI areas were evaluated against 10 CFR Part 20,

10 CFR Part 72, and applicable licensee procedures. Documents reviewed are listed in

Section 4OA5 of the Attachment

Enclosure

25

b. Findings

No findings of significance were identified.

.2 (Closed) Unresolved Item (URI) 05000338, 339/2005004-02: Inadequate Design

Control Results in Safeguards Instrument Rack Room Flood Problem

Introduction. A Green self-revealing non-cited violation was identified for inadequate

design control. Specifically, back-flow preventers were not installed in floor drains that

resulted in a flood potential for the Units 1 and 2 Safeguards Instrument Rack Rooms.

This finding was initially characterized as contrary to the requirements of 10 CFR 50,

Appendix B, Criterion XVI, Corrective Action. Subsequent review resulted in a finding

which was contrary to the requirements of Criterion III, Design Control.

Discussion. On July 9, 2005, back flush of control room chiller service water strainers

2-HV-S-1A and 1B as directed by engineering transmittal, ET N-05-0034, Operability of

2-HV-P-22C, Service Water Pump for 2-HV-E-4C, was performed in the Unit 2 air

conditioning chiller room (ACCR). Following this work activity, the licensee observed

water around a floor drain in the adjacent air conditioning fan rooms (ACFR), and

initiated Plant Issue N-2005-2565 to evaluate the abnormal condition. Subsequently,

the licensee determined that back-flow preventers were not installed in the floor drains

on the ACFRs on both units. This design requirement is necessary to ensure the

functionality of the flood walls between the ACCR and adjacent ACFR on Units 1 and 2.

Therefore, the licensee initiated a flood watch, declared the flood walls inoperable, and

entered a Yellow six-day maintenance rule risk condition based on the unavailability of

the flood walls to perform their function. The ACFRs on both units are adjacent and

open to the safeguards instrument rack rooms, which contain the solid state protection

system (SSPS) and process instrumentation and are at a two feet lower elevation. Each

instrument rack room has a sump with two pumps rated at 40 gpm each. On Unit 2, the

sump pumps discharge line is hard-piped directly to the ACCR sump. However, on Unit

1 the sump pumps discharge line is routed to a drain funnel interconnected to the floor

drain system of the adjacent ACFR. The licensee determined that this funnel did not

have a back-flow preventer installed and initiated Plant Issue N-2005-2597. Calculation

ME-0782 was performed by the licensee to evaluate the consequences of a service

water line break in either the Unit 1 or 2 ACCR. The calculation concluded that the peak

flow rate from the Units 1 and 2 ACCR to the adjacent ACFR via the floor drain piping

was 182.9 gpm and 169.4 gpm respectively, which exceeds the capacity of the sump

pumps.

The inspectors reviewed the licensees corrective action database and determined that

on October 15, 2004, Plant Issue N-2004-4554 was initiated due to water discharge

from a capped floor drain outside of the ACCR. An other evaluation was assigned to

engineering to review this condition for impact on the flood protection assumed for the

ACCR and connecting areas as applicable. This evaluation did not identify and correct

the absence of back-flow preventers in the adjacent ACFR floor drains. The inspectors

also identified the following related Plant Issues that did not result in the identification

and correction of this problem:

Enclosure

26

  • N-1999-3405, which documented operational experience from Three Mile Island

regarding check valves missing from floor drains and the impact on flood

protection; and,

  • N-1990-0020, IN 83-44-S1: Potential damage to redundant safety equipment as

a result of backflow through the equipment and floor drain system.

The inspectors concluded that the failure to install the back-flow preventers is contrary

to the requirements of 10 CFR 50, Appendix B, Criterion III, which requires in part that

measures shall be established to assure the design basis for those structures, systems

and components (SSCs) to which this appendix applies are correctly translated into

specifications, drawings, and procedures.

Analysis. The inspectors determined that the finding had a credible impact on safety

based on the potential for flooding to impact both trains of SSPS cabinets used for

engineered safeguards. The inspectors referenced IMC 0612 and determined that if left

uncorrected this finding would result in a more significant safety concern and is

consequently more than minor. Based on a review of IMC 0609 for the SDP, the

inspectors determined the finding would require a Phase III evaluation due to the loss or

degradation of equipment specifically designed to mitigate a flooding event and the

impact on two trains of a safety system. This evaluation concluded that the

performance deficiency was of very low safety significance (Green) based on the

existence of high level alarms for the associated sumps and the response time allowed

for an operator to isolate the leak (approximately 40 minutes). The inspectors also

concluded that this finding has aspects relating to the cross-cutting area of problem

identification and resolution in that the licensee had multiple opportunities to identify the

condition in their corrective action program (i.e. plant issues N-1990-0020,

N-1999-3405, and N-2004-4554).

Enforcement. 10 CFR 50, Appendix B, Criterion III, Design Control, requires in part that

measures shall be established to assure the design basis for those SSCs to which this

appendix applies are correctly translated into specifications, drawings, and procedures.

Contrary to the above, the licensee failed to ensure that back-flow preventers were

installed in the Unit 1 and 2 ACFRs to ensure the functionality of the flood walls and

safety-related instrumentation in the SSPS rack rooms. This violation is characterized

as a Green NCV and is identified as NCV 05000338, 339/2006002-02, Inadequate

Design Control Results in Safeguards Instrument Rack Room Flood Problem. This

finding is in the licensee's corrective action program as Plant Issue N-2005-2565. URI

05000338, 339/2005004-02, Inadequate Corrective Action Results in Safeguards

Instrument Rack Room Flood Problem, is closed.

Enclosure

27

4OA6 Meetings, including Exit

.1 Exit Meeting Summary

An exit meeting was conducted on January 27, 2006 to discuss the findings of the

biennial Licensed Operator Requalification Program inspection. The inspectors

confirmed that proprietary information was reviewed but is not contained in this report.

Two interim exit meetings were conducted on March 17 and March 24, 2006 with the

site vice-president and ISI/Engineering managers. Additionally, an exit was conducted

on March 30, 2006 to discuss the findings of the Radiation Protection Baseline

Inspection.

On April 11, 2006, the Senior Resident Inspector and the Chief of Reactor Projects

Branch 5 presented the inspection results for the routine integrated quarterly report to

Mr. Jack Davis and other members of the staff. The licensee acknowledged the

findings. The inspectors confirmed that proprietary information was not provided or

examined during the inspection.

.2 Annual Assessment Meeting Summary

On April 18, 2006, the NRC Chief of Reactor Projects Branch 5 met with Virginia Electric

and Power Company to discuss the NRCs Reactor Oversight Process (ROP) and the

North Anna Power Station annual assessment of safety performance for the period of

January 1, 2005 - December 31, 2005. The major topics addressed were the NRCs

assessment program and the results of the North Anna Power Station assessment.

Attendees included North Anna Power Station site management and members of site

staff.

This meeting was open to the public. The presentation material used for the discussion

is available from the NRCs document system (ADAMS) as accession number

ML061140047. ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

4OA7 Licensee-Identified Violation

The following finding of very low safety significance was identified by the licensee and is

a violation of NRC requirements which meets the criteria of Section VI of the NRC

Enforcement Policy, NUREG-1600, for being dispositioned as an NCV.

TS 5.4.1 requires that written procedures shall be established, implemented, and

maintained covering the activities in the applicable procedures recommended by

Regulatory Guide 1.33, Revision 2, Appendix A, February 1978, of which part 9.a.

requires procedures for performing maintenance. Contrary to the above, on January 6,

2006, the licensee failed to establish adequate procedure steps in maintenance

procedures 0-MCM-0103-01, "Repair of the Charging and High Head Safety Injection

Pump, and 0-MCM-0103-04, Disassembly, Inspection and Repair of

Westinghouse/Nuttall Type SU High Speed Gear Drives (Charging Pump Speed

Enclosure

28

Increaser). This resulted in tight clearances between the bearing/shaft clearances and

a failure to drain and clean the oil side of the lube oil cooler.

Debris, later found in the lube oil cooler, in conjunction with the tight clearances

subsequently led to a forced shutdown of 2-CH-P-1A (A Charging Pump, Unit 2) from

high vibration due to impending bearing failure. The inspectors reviewed IMCs 0612

and 0609 and determined that the finding was of very low safety significance given the

availability of the other charging pumps. The licensee has this finding documented in

their corrective action program as Plant Issue N-2006-0154.

ATTACHMENT: SUPPLEMENTAL INFORMATION

Enclosure

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee personnel

W. Anthes, Assistant Manager, Maintenance

G. Bischof, Director, Nuclear Safety and Licensing

J. Breeden, Supervisor, Radioactive Analysis and Material Control

W. Corbin, Director, Nuclear Engineering

J. Crossman, Assistant Manager, Nuclear Operations

J. Davis, Site Vice President

E. Dryer, Health Physicist

J. Eastwood, Corporate ISI Coordinator

R. Evans, Manager, Radiological Protection

R. Foster, Supply Chain Manager

E. Holloway, ISI

S. Hughes, Manager, Nuclear Operations

P. Kemp, Supervisor, Nuclear Safety & Licensing

J. Kirkpatrick, Manager, Maintenance

S. Kotowski, Engineering Supervisor

A. Kozak, Simulator Support Operations

L. Lane, Director, Operations and Maintenance

M. Lane, Supervisor Health Physics Operations

J. Leberstien, Licensing Technical Advisor

T. Maddy, Manager, Nuclear Protection Services

M. Main, Component Engineer

T. Mayer, Corporate Eddy Current Level III Examiner

C. McClain, Manager, Organizational Effectiveness

F. Mladen, Manager, Nuclear Site Services

B. Morrison, Assistant Engineering Manager

J. Rayman, Emergency Planning Supervisor

H. Royal, Manager, Nuclear Training

G. Salomone, Licensing

M. Sartain, Manager, Nuclear Engineering

J. Scott, Supervisor, Nuclear Training (operations)

W. Shura, Nuclear Training Supervisor

R. Wesley, Supervisor Shift Operations

M. Whalen, Licensing

R. Williams, Component Engineer

NRC personnel

K. Landis, Chief, Branch 5, Division of Reactor Projects, Region II

Attachment

A-2

LIST OF ITEMS OPENED, CLOSED AND DISCUSSED

Closed

05000338, 339/2005004-02 URI Inadequate Corrective Action Results in

Safeguards Instrument Rack Room Flood Problem

(Section 4OA5)

Opened and Closed

05000338, 339/2006002-01 NCV Failure to translate TS operable-operability

definition regarding hazard barriers into instructions

as required by 10 CFR 50 Appendix B Criterion III

(Section 1R13)

05000338, 339/2006002-02 NCV Inadequate Design Control Results in Safeguards

Instrument Rack Room Flood Problem (Section

4OA5)

Attachment

A-3

LIST OF DOCUMENTS REVIEWED

Section 1R05: Fire Protection

Plant Issues

  • N-2006-1588, NRC identified problem with oil and solvent staged in containment

beyond the specified amount identified on the transient combustible permit

Section 1R08: Inservice Inspection (ISI) Activities

Documents for Nondestructive Examination

  • NDE-UT-812, Ultrasonic Examination of Austenitic Piping Welds in Accordance

with ASME Section XI, Appendix VIII, Revision 0

  • NDE-UT-811, Ultrasonic Examination of Ferritic Piping Welds in Accordance with

ASME Section XI, Appendix VIII, Revision 0

Revision 3

  • NDE-MT-701, Magnetic Particle Examination, Revision 4
  • NASES-6.23, Boric Acid Corrosion Control Program (BACCP), Revision 2
  • DNAP-1004, Boric Acid Corrosion Control Program (BACCP), Revision 3
  • 1-PT-48.5, Leakage Inspection Above Reactor Vessel Head, Revision 1
  • 1-PT-48.4, Bare Metal Inspection of Vessel BMI Nozzles, Revision 1
  • 1-PT-48.3, Visual Inspection Borated Systems in Containment, Revision 1

1-PT-48.1, Visual Inspection of ASME XI Class 2 Pressure Boundary

Components Inside Reactor Containment, Revision 2

  • 1-PT-48, Visual Inspection of Reactor Coolant Pressure Boundary Components,

Revision 13

  • 1-PT-46.21, RCS Pressure Boundary Components Affected by Boric Acid

Accumulation, Revision 15

  • Boric Acid Corrosion Control Program Health Report, 2005-Q4
  • Areva Document No. 54-ISI-400, Multi-Frequency Eddy Current Examination of

Tubing, Revision 14

  • Areva Document No. 1275114, Eddy Current Data Management Guidelines,

Revision 07

Program, Revision 21

  • Maintenance Vendor Procedure 03-6033813A, Field Procedure for Removal and

Installation of Primary Steam Generator Manway Insert for Dominion Generators,

Revision 2

  • Areva Document Identifier 51-9014652, North Anna Unit 1 1R18 - EPRI

Appendix H Eddy Current Technique Review

  • Confined Space Evaluation and Entry Permit - Hot and Cold Legs
  • Foreign Material Control Log
  • Eddy Current Analyses Calibration No. 11 for tubes R18C16, R16C16, and

R16C17; 47 for tube R29C51; and 48 for tubes R24C58 and R03C58

Attachment

A-4

  • Data Aquisition and Analysis Personnel Qualification for Level II Data Operators,

Level II A and Level III A Analysts

Plant Issues

  • N-2005-5615, Initiate evaluation of the effectiveness of the boric acid corrosion

control program

  • N-2006-1030, Listing of boric acid leaks identified during 1-PT-46.21 walkdown
  • N-2006-1082, Boron crystals on Unit 1 reactor head thermocouples
  • N-2006-1090, Valves discovered with boric acid during 1-PT-48 walkdown
  • N-2006-1204, High number of boric acid leaks identified
  • N-2005-5399, Boric acid leakage through canopy seal weld on SI sampling valve
  • N-2006-1357, Deviation in the standard for the signal amplitude between

standards ADVB-013-96 and ADVB-016-96

Section 1R11: Licensed Operator Requalification - Biennial Review

Documents

  • Functional Implementation Guideline (FIG) -07 Implementing LORP Instructional

/Evaluation Components, Revision 5

  • FIG - 07, Program Administration and Documentation, Revision 11
  • FIG - 09, Administering the LORP Examination Banks (test items and task

performance evaluations), Revision 16

  • DNAP-0509, Dominion Nuclear Procedure Adherence and Usage Revision 4
  • TRCP-3002, Simulator Modification Record Process (SMR), Revision 9
  • TRCP-3006, Simulator Configuration Management, Revision 6
  • TRCP 3007, Simulator Performance Testing, Revision 1
  • Executive Summary-Simulator Performance Test Procedure, January 2006
  • NAS-RC-01 System Test Procedure, Revision 0
  • Memo Dated January 13, Simulator Review Board Minutes
  • Various Simulator Modification Requests (SMR)
  • Scenario SXG #44, Revision 3
  • Scenario SXG #31, Revision 4

Recirculation Fans on the backboards watchstation. (10/12/05)

  • JPM - N1473/14045 Rack in a 4160 Volt Breaker (10/12/05)

generators by way of the hand control valve header (10/12/05)

  • Badge Access Transaction Reports for Reactivation of Licenses (3)
  • Licensed Operator Medical Records (20)
  • Feedback Summaries

Attachment

A-5

Section 1R12: Maintenance Effectiveness

Plant Issues

  • N-2005-1050, identification by engineering that the process used in the

manufacture of EXIDE type 3CC-7 batteries may result in premature degradation

of the battery

  • N-2005-1165,internal resistance reading obtained on the 1J EDG battery indicate

the cell may be degraded

  • N-2006-0357, maintenance rule criteria exceeded for SBO diesel generator
  • N-2006-0387, internal resistance readings obtained for the 1JEDG batteries

were higher than those obtained previously

Section 1R13: Maintenance Risk Assessments and Emergent Work Evaluation

Plant Issues

  • N-2006-1174, NRC identified problem with a failure to assess risk for

2-CC-TV-204B; subsequent calculations resulted in a Green risk condition.

Section 1R20: Refueling and Other Outages

Documents

  • Procedure 1-GOP-13.0, Alternate Core Cooling Method Assessment
  • Dominion Memorandum dated 3/6/06, 2006 Outage Plan Safety Review North

Anna Unit 1

  • VPAP-2805, Shutdown Risk Program

NRC identified Plant Issues from Containment Closeout Inspection

  • N-2006-2076, snubber 1-RC-HSS-838 was bound in place by a support on one

side and insulation on the other side

  • N-2006-2077, dry boric acid around packing gland for 1-RC-HCV-1556A
  • N-2006-2079, insulation issues were identified on several components: 1-BD-1,

1-HC-343, 1-CH-366, 1-RC-199, 1-CH-365, 1-CC-716, 1-CC-944, 1-CC-45,

sample system line in mechanical penetration area, 1-RH-E-1B, A SG

blowdown line on RHR flat

  • N-2006-2080, boric acid identified on packing gland for 1-CH-TV-1204A
  • N-2006-2081, BACC flag found on 1-IA-38
  • N-2006-2083, miscellaneous material and debris was identified and removed

from containment including: several large screwdrivers, pieces of tape &

tie-wraps, 5 large washers, piece of cloth, loose insulation, cup of paint chips

  • N-2006-2084, metal filings and dirt was identified on the 4160V electrical lead

insulators in the containment penetration area for 1-RC-P-1B, 1-RC-P-1C, and

1-RC-P-1A

  • N-2006-2085, 2 openings in the screen installed to prevent paint on containment

air recirc fan duct from reaching sump was identified near 1-HV-F-1A

  • N-2006-2087, the inspector informed the licensee that the UFSAR required

encapsulation of all insulation, yet licensees procedure, NAI-029, Specification

for Installation of Thermal Insulation, allows for insulation in SG cubicles to be

left unjacketed if certain criteria are met

Attachment

A-6

Section 2OS1: Access Controls to Radiologically Significant Areas

Procedures, Manuals, and Guidance Documents

  • Health Physics Administrative Procedure HPAP-1081, Radiation Work Permit

Program, Revision 4

  • C-HP-1032.060, Radiological Posting and Access Control, Revision 1
  • C-HP-1061.020, Personnel Contamination Monitoring and Decontamination,

Revision 8

  • C-HP-1081.010, Radiation Work Permits: Preparing and Approving, Revision 7
  • C-HP-1081.020, Radiation Work Permits: RWP Briefing and Controlling Work,

Revision 5

  • C-HP-1081.040, Radiation Work Permits: Providing HP Coverage During Work,

Revision 1

  • HP-1071.020, Controlling Contaminated Material, Revision 6
  • Standing Order #125, Compensatory measures implemented for the use of

RMS, 8/15/05

Radiation Work Permits

  • 05-2-1102, Load, transport, and store spent fuel dry storage casks
  • 06-2-3503, Replace transfer canal blank flange and transfer cart inspection
  • 06-2-3507, Vacuum debris from cavity/transfer canal during refueling operations,

perform decon of transfer canal

  • 06-2-3230, Walkdowns, inspections, and observations

examination for inservice inspection program

  • 06-2-1502, Containment entry during subatmospheric conditions
  • 06-2-1210, Spent resin transfer

Surveys, Data, Records

  • Plant Status Board Radiological Surveys (3/13/06-3/17/06, 3/27/06-3/29/06)
  • High Radiation Key Locker Log, printed 3/8/06
  • Whole Body Count and Inhalation Intake Data Sheets, TLD 3020, 10/14/05
  • Special Dosimetry Issue Worksheets, TLDs 6021 and 7625, 3/20/06

Audits and Self-Assessments

  • ITC-SA-04-02, Assessment of Nuclear Business Unit for Adverse Trends in

Radiological Protection Events, 4/29/04

  • Nuclear Oversight Audit Report 05-06, Radiological Protection, Process Control

Program, and Chemistry Program at Millstone, North Anna, and Surry,

05/09/2005 - 05/27/2005

Attachment

A-7

CAP Documents (Plant Issues)

  • N-2005-3958, Worker received dose rate alarm while working under Unit 2

reactor vessel, 10/3/05

  • N-2005-4038, Lock for B motor cube door on 262' of Unit 2 containment is

broken. Currently this door is being controlled as a locked high radiation area.,

10/5/05

  • N-2005-4099, Supplemental information to document events propagated from a

Level 1 PCE; 8,000 dpm in facial area, 10/6/05

  • N-2005-4389, Individual received a DAD dose rate alarm while working on

scaffold platform in B cube 241', 10/13/05

  • N-2005-4657, Worker received dose rate alarm while performing

deconatmination activities in Unit 2 reactor cavity, 10/21/05

  • N-2006-1001, Decon Building basement high radiation gate locks have been

found to be defective 8 times in the last 24 months, 3/9/06

  • N-2006-1336, An HP technician received a dose alarm while performing surveys

in Unit 1 reactor containment, 3/18/05

  • N-2006-1378, Individual received dose rate alarm while performing observations

on the scaffold platform in C cube 241', 3/19/06

  • N-2006-1462, Individual received dose rate alarm while performing valve

maintenance activities on scaffold platform in C cube 241', 3/21/06

  • N-2006-1544, Worker performing inspections in the secondary side of Unit 1 B

S/G received a dose alarm, 3/22/06

Attachment

A-8

  • 06-023, Perform Health Physics zone coverage, Surveys, and walkdowns during

the Unit 1 2006 Refueling outage.

  • 06-029, Perform AOV valve maintenance to include repack, adjustment, cut out,

and inspection of AOV's during Unit 1 2006 Refueling outage.

  • WIPAR: RWP 06-2-3241, Perform AOV maintenance during Unit 1 2006

refueling outage, 3/27/06

  • WIPAR: RWP 06-2-3204, Perform RCP maintenance during unit 2006 outage.

Includes A Seals, and annual PM's, 3/27/06

  • WIPAR: RWP 06-2-3214, Remove, replace and inspect snubbers during Unit 1

2006 refueling outage, 3/28/06

Section 2PS2: Radioactive Material Processing and Transportation

Procedures, Guidance Documents, and Manuals

  • HP-1071.021, Storing Radioactive Material Outside the Protected Area,

Revision 14

  • HP-1071.030, Receiving Radioactive Material, Revision 11
  • HP-1072.010, Packaging Radioactive Waste, Revision 9
  • HP-1072.020, Sampling, Analyzing, and Classifying Solid Radioactive Waste,

Revision 7

  • 0-HSP-INST-002, Health Physics Assessment of Radioactive Waste Stream

Changes, Revision 0

  • C-HP-1071.040, Packaging and Shipment of Radioactive Material, Revision 1

Attachment

A-9

  • C-HP-1072.040, Radioactive Waste Disposal Using the Barnwell Disposal

Facility, Revision 3

  • C-HP-1072.050, Radioactive Waste Transfer to Licensed Waste Processors,

Revision 1

Records and Data

  • 2004 and 2005 Radioactive Waste Shipment Summary Forms
  • Radioactive Material Shipment Log, 2005 and 2006 (Year-to-Date)
  • HAZMAT/Transportation Safety Qualification List, Undated

01, 2004 to December 31, 2004)

  • Flow Valve Operating Numbers Diagram (FVOND), Waste Disposal System,

North Anna Power Station - Unit 1 (NAPSU1), Drawing No. 11715-FM-87A,

Sheet 1, Revisions 26 and 27

  • FVOND, Waste Disposal System, NAPSU1, Drawing No. 11715-FM-87A, Sheet

2, Revision 30

  • FVOND, Waste Disposal System, NAPSU1, Drawing No. 11715-FM-87A, Sheet

3, Revision 33

  • FVOND, Waste Disposal System, NAPSU1, Drawing No. 11715-FM-087D,

Sheet3, Revision 33

  • New Waste Stream Data Reports, Dated 11/16/2002, 04/25/2003, 12/08/2004,

02/27/2005, 08/05/2005

  • Radwaste Shipping Package 05-DUR-05, 8/31/05
  • Radwaste Shipping Package 05-DUR-06, 12/16/05
  • Radwaste Shipping Package 05-CNS-02, 6/7/05
  • SCO Shipping Packages 05-1032 (8/17/05), 05-1046 (10/6/05), and 06-1021

(3/19/06)

Audits and Self-Assessments

  • Nuclear Oversight Audit Report 04-08: Radiation Protection & Process Control

Program, 05/17/2004 - 05/28/2004

  • Nuclear Oversight Audit Report 05-06: Radiation Protection/Process

Control/Chemistry Programs, 05/09/2005 - 05/27/2005

CAP Documents (Plant Issues)

  • N-2004-1182, Repetitive failures are occurring on the discharge line for

2-DA-P-7B, Unit 2 inside Mat Sump pump, 04/15/2004

  • N-2004-1788, Spent OLCMS secondary resin (which was counted in two

separate marinelli containers) was released for disposal to clean trash,

05/16/2004

  • N-2005-2366, An upward trend in dose rates around the Fluid Waste Treatment

Tank has been noticed by HP during routine radiological surveys.

  • N-2005-2586, contrary to the requirements of 49 CFR Subpart H Code of

Federal Regulations, Transportation, a Facilities and Support personnel has

been transporting hazardous material (gasoline and diesel fuel) offsite without

completing employer HAZMAT training.

Attachment

A-10

  • N-2005-3345, Upon completion of the final pump down of the Fluid Waste

Treatment Tank, dose rates in the area increased to 300-500 mr/hr around the

tank.

Section 4OA1: Performance Indicator Verification

Procedures, Manuals, and Guidance Documents

  • VPAP 1501, Deviations, Revision 17

Records and Data

  • EPD Dose/Dose Rate Alarms: July 2005 - March 2006
  • NAPS NRC Performance Indicator Data: January 2005 - January 2006
  • North Anna Power Station Units 1 and 2 and ISFSI Annual Radioactive Effluent

Release Report for Calendar Year 2004, dated 4/14/05

  • Quarterly printouts for Liquid and Gaseous Effluent doses to members of the

public, January - December 2005

CAP Documents (Plant Issues)

  • Review of all Plant Issues from July 1, 2005 to March 18, 2006 with search terms

DAD Dose Rate Alarm, Dose Rate Alarm, Dose Rate, DAD, and

dosimeter. Detailed review and discussion with licensee of Plant Issues listed

in Section 2OS1 of the Attachment.

Section 4OA5: Other Activities

ISFSI Radiological Controls

Procedures

  • HP-1020.012, Radiological Protection Action Plan During Dry Storage Cask

Activities, Revision 014

  • 0-Health Physics Surveillance (HPS)-ISFSI-001, Independent Spent Fuel

Storage Installation (ISFSI) Health Physics TLD Survey Surveillance, Revision 3

Surveys, Data, and Records

  • ALARA Package 05-003, Load, transport, and store spent fuel dry storage cask
  • Cask TN-32 #47 load, transport, and placement surveys (4/5/05-4/14/05)
  • ISFSI Pad surveys (2/17/04, 5/21/04, 8/22/04, 11/19/04, 8/24/05 11/23/05,

2/21/06)

  • Cask TN-32 #42 Grid Survey, 2/7/04
  • Cask TN-32 #43 Grid Survey, 3/13/04
  • Cask TN-32 #45 Grid Survey, 6/21/04
  • ISFSI Environmental Monitoring Results - TLD data (4th quarter 2004 - 3rd quarter

2005)

CAP Documents (Plant Issues)

  • N-2004-2910, Some discrepancies between TLD readouts and calculated

neutron exposures were noted on the 1st quarter 2004 TLDs, 8/4/04

  • N-2004-4993,While performing ISFSI perimeter fence survey as part of the

quarterly Controlled Area Survey, noted that a jersey barrier was located directly

between the northernmost ISFSI TLD and the SF casks, 11/19/04

  • N-2005-1326, During spent fuel cask activities, 4 bubble dosimeters used to

estimate neutron exposure, did not respond as expected, 4/6/05

Attachment

A-11

LIST OF ACRONYMS

ALARA As Low As Reasonably Achievable

ASME American Society of Mechanical Engineers

BACCP Boric Acid Corrosion Control Program

CAP corrective action program

CC component cooling

DOT Department of Transportation

ED electronic dosimeter

EDG emergency diesel generator

EPRI Electric Power Research Institute

HPT health physics technician

HRA high radiation area

Hx heat exchanger

IMC inspection manual chapter

ISFSI Independent Spent Fuel Storage Installation

ISI inservice inspection

JPMs Job Performance Measures

LHRA locked high radiation area

LHSI Low Head Safety Injection

LOCA Loss of Coolant Accident

NCV non-cited violation

NDE nondestructive examination

PCP Process Control Program

PREACS Emergency Core Cooling System Pump Room Exhaust Air Clean-up System

RAB reactor auxiliary building

RCA radiologically controlled area

RCB reactor containment building

RCP reactor coolant pump

RCS reactor coolant system

RFO Refueling Outage

RSST Reserve Station Service Transformer

RWP Radiation Work Permit

SDP Significance Determination Process

S/G steam generator

SSC structures, systems, and components

SSPS solid state protection system

TS Technical Specifications

UFSAR Updated Final Safety Analysis Report

VHRA very high radiation area

VPAP Virginia Power Administrative Procedure

WO Work Order

Attachment