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Category:Inservice/Preservice Inspection and Test Report
MONTHYEARML24296B1902024-10-22022 October 2024 10 CFR 50.55a Requests for the Fifth Ten-Year Interval Inservice Testing Program ML24248A2492024-09-0404 September 2024 Inservice Inspection Program Fourth Interval, Third Period, Refueling Outage 26 Owner’S Activity Report ML23277A2772023-10-11011 October 2023 Regulatory Audit Summary Concerning Review of Request Number CI3R-01 for Proposed Alternative Inspection Frequency for Containment Unbonded Post Tensioning System Components ML23075A0742023-03-16016 March 2023 Containment Inservice Inspection Program Third Interval, Second Period, Refueling Outage 25 Owner’S Activity Report ML23075A1632023-03-16016 March 2023 Inservice Inspection Program Fourth Interval, Third Period, Refueling Outage 25 Owner’S Activity Report ML22124A0062022-05-0505 May 2022 Review of the Spring 2021 Refueling Outage 24 Steam Generator Tube Inservice Inspection Report ET 21-0009, Results of the Steam Generator Tube Inservice Inspection During the 24th Refueling Outage2021-11-0101 November 2021 Results of the Steam Generator Tube Inservice Inspection During the 24th Refueling Outage ML21217A3342021-08-0505 August 2021 Inservice Inspection Program Fourth Interval, Second Period, Refueling Outage 24 Owner'S Activity Report ML21217A3352021-08-0505 August 2021 Containment Inservice Inspection Program Third Interval, First Period, Refueling Outage 24 Owner'S Activity Report ML20042C8922020-02-0404 February 2020 Containment Inservice Inspection Program Third Interval, First Period, Refueling Outage 23 Owner'S Activity Report ML20042C8962020-02-0404 February 2020 Lnservice Inspection Program Fourth Interval, Second Period, Refueling Outage 23 Owner'S Activity Report ET 18-0029, (WCGS) - Results of the Twenty First Steam Generator Tube Inservice Inspection2018-10-31031 October 2018 (WCGS) - Results of the Twenty First Steam Generator Tube Inservice Inspection ML18234A1312018-08-14014 August 2018 Lnservice Inspection Program Fourth Interval, First Period, Refueling Outage 22 Owner'S Activity Report ML18234A1322018-08-14014 August 2018 Submittal of Containment Inservice Inspection Program Second Interval, Third Period, Refueling Outage 22 Owner'S Activity Report ET 17-0008, Results of the Twentieth Steam Generator Tube Lnservice Inspection2017-05-0202 May 2017 Results of the Twentieth Steam Generator Tube Lnservice Inspection ET 17-0007, CFR 50.55a Request 14R-05 for the Fourth Inservice Inspection Program Interval2017-04-13013 April 2017 CFR 50.55a Request 14R-05 for the Fourth Inservice Inspection Program Interval ET 16-0005, Inservice Inspection Plan and 10 CFR 50.55a Requests 14R-01 and 14R-02 for the Fourth Inservice Inspection Program Interval2016-02-23023 February 2016 Inservice Inspection Plan and 10 CFR 50.55a Requests 14R-01 and 14R-02 for the Fourth Inservice Inspection Program Interval ET 15-0024, Results of the Nineteenth Steam Generator Tube Inservice Inspection2015-10-20020 October 2015 Results of the Nineteenth Steam Generator Tube Inservice Inspection ET 15-0022, Fourth Ten-Year Interval Submittal Snubber Program Plan and Inservice Testing Program Plan, WCOP-29, Revision 02015-09-0202 September 2015 Fourth Ten-Year Interval Submittal Snubber Program Plan and Inservice Testing Program Plan, WCOP-29, Revision 0 ML15217A0222015-07-28028 July 2015 Containment Inservice Inspection Program Second Interval, Second Period, Refueling Outage 20 Owner'S Activity Report ML15222A2512015-07-28028 July 2015 Inservice Inspection Program Third Interval, Third Period, Refueling Outage 20 Owner'S Activity Report ET 14-0018, 10CFR50.55a Request I3R-10 for Third Inservice Inspection Program Interval2014-06-26026 June 2014 10CFR50.55a Request I3R-10 for Third Inservice Inspection Program Interval ML14174B1232014-06-25025 June 2014 Review of 18th Steam Generator Tube Inspection Report ET 13-0030, Results of the Eighteenth Steam Generator Tube Inservice Inspection2013-09-30030 September 2013 Results of the Eighteenth Steam Generator Tube Inservice Inspection ML13199A2362013-07-11011 July 2013 Submittal of Containment Inservice Inspection Program Second Interval, Second Period, Refueling Outage 19 Owner'S Activity Report ET 11-0008, (WCGS) - Results of the Seventeenth Steam Generator Tube Inservice Inspection2011-10-19019 October 2011 (WCGS) - Results of the Seventeenth Steam Generator Tube Inservice Inspection ML11263A1492011-09-13013 September 2011 Containment Inservice Inspection Program Second Interval, First Period, Refueling Outage 18 Owner'S Activity Report ML11263A1482011-09-13013 September 2011 Inservice Inspection Program Third Interval, Second Period, Refueling Outage 18 Owner'S Activity Report ET 10-0012, Results of the Sixteenth Steam Generator Tube Inservice Inspection2010-04-0808 April 2010 Results of the Sixteenth Steam Generator Tube Inservice Inspection ML1004907522010-02-0909 February 2010 Submittal of Inservice Inspection Program Third Interval, Second Period, Refueling Outage 17 Owner'S Activity Report ML0822603672008-08-0606 August 2008 Containment Inservice Inspection Program First Interval, Third Period, Owner'S Activity Reports ML0822603412008-08-0606 August 2008 Inservice Inspection Program Third Interval, First Period, Refueling Outage 16 Owner'S Activity Report ML0704304622007-01-31031 January 2007 Containment Inservice Inspection Program First Interval, Third Period, Refueling Outage 15 Owner'S Activity Report RA-07-0012, Inservice Inspection Program Third Interval, First Period, Refueling Outage 15 Owner'S Activity Report2007-01-31031 January 2007 Inservice Inspection Program Third Interval, First Period, Refueling Outage 15 Owner'S Activity Report ML0614503192006-05-19019 May 2006 10 CFR 50.55a Request I3R-05, Installation and Examination of Full Structural Weld Overlays for Repairing/Mitigating Pressurizer Nozzle-to-Safe End Dissimilar Metal Welds and Adjacent Safe End-to Piping Stainless Steel Welds ET 06-0011, CFR 50.55a Requests I2R-34, I2R-35, I2R-36, I2R-37, and I2R-38 for the Second Inservice Inspection Program Interval2006-03-0202 March 2006 CFR 50.55a Requests I2R-34, I2R-35, I2R-36, I2R-37, and I2R-38 for the Second Inservice Inspection Program Interval ET 06-0010, Inservice Inspection Program Plan for the Third Ten-Year Interval and 10 CFR 50.55a Requests I3R-01, I3R-02, and I3R-042006-03-0202 March 2006 Inservice Inspection Program Plan for the Third Ten-Year Interval and 10 CFR 50.55a Requests I3R-01, I3R-02, and I3R-04 ET 06-0001, Revision to Technical Specification 5.5.8, Inservice Testing Program to Adopt Technical Specification Task Force Standard Technical Specification Change Traveler, TSTF-479, Revision 02006-02-0101 February 2006 Revision to Technical Specification 5.5.8, Inservice Testing Program to Adopt Technical Specification Task Force Standard Technical Specification Change Traveler, TSTF-479, Revision 0 ET 05-0004, Steam Generator Tube Plugging Report2005-05-0404 May 2005 Steam Generator Tube Plugging Report WM 04-0046, Results of the Twelfth Steam Generator Tube Inservice Inspection2004-10-27027 October 2004 Results of the Twelfth Steam Generator Tube Inservice Inspection WM 04-0008, Request to Extend the Second 10-year Inservice Inspection (ISI) Interval for Reactor Pressure Vessel Examinations, 10 CFR 50.55a Request 12R-282004-04-15015 April 2004 Request to Extend the Second 10-year Inservice Inspection (ISI) Interval for Reactor Pressure Vessel Examinations, 10 CFR 50.55a Request 12R-28 ET 03-0006, Implementation of the ASME Code for Operation and Maintenance of Nuclear Power Plants, Regarding the Check Valve Monitoring Program2003-08-26026 August 2003 Implementation of the ASME Code for Operation and Maintenance of Nuclear Power Plants, Regarding the Check Valve Monitoring Program ML0319704482003-07-0808 July 2003 Inservice Inspection Program Second Interval, Second Period Owner'S Activity Reports ET 02-0046, Results of Eleventh Steam Generator Tube Inservice Inspection2002-12-11011 December 2002 Results of Eleventh Steam Generator Tube Inservice Inspection ET 02-0049, Containment Inservice Inspection Program First Interval, First Period Owner'S Activity Reports2002-11-0404 November 2002 Containment Inservice Inspection Program First Interval, First Period Owner'S Activity Reports 2024-09-04
[Table view] Category:Letter
MONTHYEARIR 05000482/20244202024-10-31031 October 2024 Security Baseline Inspection Report 05000482/2024420 ML24296B1902024-10-22022 October 2024 10 CFR 50.55a Requests for the Fifth Ten-Year Interval Inservice Testing Program 05000482/LER-2024-001-01, Mode 3 Entry with One Auxiliary Feedwater Pump Train Inoperable Due to Missed Post-Maintenance Testing2024-10-22022 October 2024 Mode 3 Entry with One Auxiliary Feedwater Pump Train Inoperable Due to Missed Post-Maintenance Testing 05000482/LER-2024-002, Technical Specification Required Shutdown Due to Inoperable Auxiliary Feedwater Discharge Valve2024-10-21021 October 2024 Technical Specification Required Shutdown Due to Inoperable Auxiliary Feedwater Discharge Valve ML24284A2842024-10-10010 October 2024 (Wcgs), Revision of One Form That Implements the Radiological Emergency Response Plan (RERP) ML24283A0752024-10-0909 October 2024 Notification of Commercial Grade Dedication Inspection (05000482/2025012) and Request for Information ML24199A1712024-09-17017 September 2024 Issuance of Amendment No. 241 Revise Ventilation Filter Testing Program Criteria and Administrative Correction of Absorber in Technical Specification 5.5.11 ML24260A0712024-09-12012 September 2024 License Amendment Request for a Risk-Informed Resolution to GSI-191 IR 05000482/20240102024-09-10010 September 2024 Biennial Problem Identification and Resolution Inspection Report 05000482/2024010 (Public) ML24255A8642024-09-0606 September 2024 Rscc Wire & Cable LLC Dba Marmon Industrial Energy & Infrastructure - Part 21 Retraction of Final Notification ML24248A0762024-09-0404 September 2024 Containment Inservice Inspection Program Third Interval, Second Period, Refueling Outage 26 Owner’S Activity Report ML24248A2492024-09-0404 September 2024 Inservice Inspection Program Fourth Interval, Third Period, Refueling Outage 26 Owner’S Activity Report ML24241A2212024-08-29029 August 2024 Notice of Enforcement Discretion for Wolf Creek Generating Station ML24240A2642024-08-27027 August 2024 Corporation - Request for Notice of Enforcement Discretion Regarding Technical Specification 3.7.5, Auxiliary Feedwater (AFW) System ML24239A3972024-08-23023 August 2024 Rssc Wire & Cable LLC Dba Marmon - Part 21 Final Notification - 57243-EN 57243 IR 05000482/20240052024-08-14014 August 2024 Updated Inspection Plan for Wolf Creek Generating Station (Report 05000482/2024005) ML24227A5562024-08-14014 August 2024 Application to Revise Technical Specifications to Adopt TSTF-569-A, Revision 2, Revision of Response Time Testing Definitions ML24213A3352024-07-31031 July 2024 License Amendment Request to Revise Technical Specification 3.2.1, Heat Flux Hot Channel Factor (Fq(Z)) (Fq Methodology), to Implement the Methodology from WCAP-17661-P-A, Revision 1. ML24206A1252024-07-24024 July 2024 Revision of Three Procedures and Two Forms That Implement the Radiological Emergency Response Plan (RERP) IR 05000482/20240022024-07-18018 July 2024 Integrated Inspection Report 05000482/2024002 05000482/LER-2024-001, Mode 3 Entry with One Auxiliary Feedwater Pump Train Inoperable Due to Missed Post-Maintenance Testing2024-07-0202 July 2024 Mode 3 Entry with One Auxiliary Feedwater Pump Train Inoperable Due to Missed Post-Maintenance Testing IR 05000482/20244012024-07-0202 July 2024 Security Baseline Inspection Report 05000482/2024401 ML24178A3672024-06-26026 June 2024 Correction to 2023 Annual Radioactive Effluent Release Report – Report 47 ML24178A4142024-06-26026 June 2024 Revision of One Procedure and One Form That Implement the Radiological Emergency Response Plan (RERP) ML24162A1632024-06-11011 June 2024 Operating Corporation – Notification of Biennial Problem Identification and Resolution Inspection and Request for Information (05000482/2024010) ML24150A0562024-05-29029 May 2024 Foreign Ownership, Control or Influence (FOCI) Information – Change to Lists of Owners, Officers, Directors and Executive Personnel - Form 405F Amendment ML23345A1602024-05-0909 May 2024 Revision of Safety Evaluation for Amendment No. 237 Request for Deviation from Fire Protection Requirements ML24089A2622024-04-29029 April 2024 Financial Protection Levels ML24118A0022024-04-27027 April 2024 Wolf Generating Nuclear Station - 2023 Annual Radiological Environmental Operating Report ML24118A0032024-04-27027 April 2024 2023 Annual Radioactive Effluent Release Report - Report 47 ML24113A1882024-04-19019 April 2024 Foreign Ownership, Control or Influence Information - Change to Lists of Owners, Officers, Directors and Executive Personnel - Form 405F Amendment ML24109A1842024-04-18018 April 2024 Cycle 27 Core Operating Limits Report ML24109A1212024-04-18018 April 2024 (WCGS) Form 5 Exposure Report for Calendar Year 2023 IR 05000482/20240012024-04-17017 April 2024 Integrated Inspection Report 05000482/2024001 ML24114A1442024-04-15015 April 2024 Redacted Updated Safety Analysis Report (WCGS Usar), Revision 37 ML24106A1482024-04-15015 April 2024 Notification of Inspection (NRC Inspection Report 05000482/2024003) and Request for Information ML24098A0052024-04-0707 April 2024 2023 Annual Environmental Operating Report ML24089A0972024-03-29029 March 2024 Response to NRC Regulatory Issue Summary 2024-01, Preparation and Scheduling of Operator Licensing Examinations ML24089A1352024-03-29029 March 2024 10 CFR 50.46 Annual Report of Emergency Core Cooling System (ECCS) Evaluation Model Changes ML24074A3312024-03-14014 March 2024 Missed Quarterly Inspection Per 40 CFR 266 Subpart N IR 05000482/20240122024-03-11011 March 2024 Fire Protection Team Inspection Report 05000482/2024012 ML24080A3452024-03-11011 March 2024 7 of the Wolf Creek Generating Station Updated Safety Analysis Report ML24016A0702024-03-0808 March 2024 Issuance of Amendment No. 240 Removal of the Power Range Neutron Flux Rate - High Negative Rate Trip Function from Technical Specifications ML24068A1992024-03-0707 March 2024 Changes to Technical Specification Bases - Revisions 93 and 94 ML24066A0672024-03-0505 March 2024 4-2022-024 Letter - OI Closure to Licensee ML24061A2642024-03-0101 March 2024 Revision of Two Procedures That Implement the Radiological Emergency Response Plan (RERP) for Wolf Creek Generating Station (WCGS) Commissioners IR 05000482/20230062024-02-28028 February 2024 Annual Assessment Letter for Wolf Creek Generating Station Report 05000482/2023006 ML24059A1702024-02-28028 February 2024 Annual Fitness for Duty Program Performance Report, and Annual Fatigue Report for 2023 ML24026A0212024-02-27027 February 2024 Issuance of Amendment No. 239 Modified Implementation Date of License Amendment No. 238 ML24050A0012024-02-19019 February 2024 (Wcgs), Revision of One Form That Implements the Radiological Emergency Response Plan (RERP) 2024-09-06
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W LF CREEK r'NUCLEAR OPERATING CORPORATION Steven R. Koenig Manager Regulatory Affairs July 28, 2015 RA 15-0062 U. S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, DC 20555
Subject:
Docket No. 50-482: Inservice Inspection Program Third Interval, Third Period, Refueling Outage 20 Owner's Activity Report Gentlemen:
Enclosed is the Wolf Creek Nuclear Operating Corporation (WCNOC) Owner's Activity Report (Form OAR-I, Report Number WCRE-16, 13-P3-RF20) for inservice inspections performed after Wolf Creek Generating Station's (WCGS) nineteenth refueling outage (RF19) that concluded on May 13, 2014, and up to, and including, WCGS' twentieth refueling outage (RF20) that concluded on May 3, 2015. RF20 was the second refueling outage of the third period of the third interval of the WCNOC Inservice Inspection Program. The enclosed report is submitted pursuant to the requirements of paragraph IWA-6240 of the 1998 Edition through 2000 Addenda of Section Xl of the American Society of Mechanical Engineers (ASME) Boiler and Pressure Vessel Code and ASME Code Case N-532-4.
This letter contains no commitments. If you have any questions concerning this matter, please contact me at (620) 364-4041 or Mr. Bill Muilenburg at (620) 364-4186.
Sincerely, for Steven R. Koenig SRK/rlt
Enclosure:
cc: M. L. Dapas (NRC), w/e C. F. Lyon (NRC), w/e N. H. Taylor (NRC), w/e/- * ) -
Senior Resident Inspector (NRC), w/e P.O. Box 411 I Burlington, KS 66839 I Phone: (620) 364-8831 An Equal Opportunity Employer M/F/HC/VET
Enclosure to RA 15-0062 Wolf Creek Nuclear Operating Corporation (WCNOC)
Owner's Activity Report (Form OAR-I, Report Number WCRE-1 6, 13-P3-RF20)
(6 pages)
FORM OAR-I OWNER'S ACTIVITY REPORT Report Number WCRE-16. 13-P3-RF20 Plant Wolf Creek Generating Station, 1550 Oxen Lane Northeast. Burlington, Kansas 66839 Unit No. 1 Commercial service date 9-3-1 985 Refueling outage no. RF-20 (if applicable)
Current inspection interval 3rd.
list, 2nd, 3rd, 4th, other)
Current inspection period 3rd list. 2nd, 3rd)
Edition and Addenda of Section XI applicable to the inspection plans 1998 Edition through 2000 Addenda Date and revision of inspection plans WCRE-16 Rev. 9. dated 2-6-13 Edition and Addenda of Section XI applicable to repair/replacement activities, if different than the inspection plans same Code Cases used: See Attachment 1 lit applicable)
CERTIFICATE OF CONFORMANCE I certify that (a) the statements made in this report are correct; (b) the examinations and tests meet the Inspection Plan as required by the ASMIE Code, Section Xh; and Cc)the repair/replacement activities and evaluations supporting the completion of RF-20 conform to the requirements of Section Xl.
(refueling outage number)
Signed Engineer Date 7/16/2015 Owner or Owner's Designee. Title CERTIFICATE OF INSERVICE INSPECTION I, the undersigned, holding a valid commission issued by the National Board of Boiler and Pressure Vessel Inspectors and the State or Province of Kansas and employed by The Hartford Steam Boiler Inspection and Insurance Co. of Connecticut have inspected the items described in this Owner's Activity Report, and state that, to the best of my knowledge and belief, the Owner has performed all activities represented by this report in accordance with the requirements of Section XI.
By signing this certificate neither the Inspector nor his employer makes any warranty, expressed or implied, concerning the repair/replacement activities and evaluation described in this report. Furthermore, neither the Inspector nor his employer shall be liable in any manner for any personal injury or property damage or a loss of any kind arising from or connected with this inspection.
___________________Commissions NB 13573 ANI KS 657 Inspector's 5ignat* 7 Notional Board, State. Province, and Endorsements Date * /( /'
OAR-I I3-P3-RF-20 Page 1 o.[6
TABLE 1 ITEMS WITH FLAWS OR RELEVANT CONDITIONS THAT REQUIRED EVALUATION FOR CONTINUED SERVICE Examination Item Description Evaluation Description Category and Item Number D-B, D2.10 EF-054-HBC-8 A through-wall leak was identified. An evaluation utilizing the methodology of ASME Code Case N-5 13-2 was performed for continued operation. The evaluation determined that structural integrity was intact and that the piping could remain in operation in the current condition until the scheduled repair during MC2O.
Periodic monitoring prior to the repair was required.
D-B, D2.10 EG-210-ITBC-24 A through-wall leak was identified. An evaluation utilizing the methodology of ASME Code Case N-513-2 was performed for continued operation. The evaluation determined that structural integrity was intact and that the piping could remain in operation in the current condition until the scheduled repair during RF20.
Periodic monitoring prior to the
____________________repair was required.
D-B, D2.10 SGNO1A, SGN01B, SGN01C, An evaluation was performed to SGNO1D address the operability of the Containment Air Coolers. The operability was in question based on an operational history of leakage. Tube failure was occurring as a result of under deposit pit corrosion that subsequently led to tube leaks.
Hydrostatic testing was performed on the tube bundles using a test pressure determined by utilizing corrosion rates and the required wall thickness.
Based on the hydrostatic testing results, the evaluation determined that the Containment Air Coolers were able to perform their design function until replacement in RF2O.
OAR-I 13-P3-RF-20 Page2of6
TABLE 2 OF REPAIR/REPLACEMENT ACTIVITIES REQUIRED FOR CONTINUJED SERVICE ABSTRACT Code Item Description of Work Date Repair/Replacement Class Description Completed Plan Number (Note 1) 3EKJ03B Cut, realign, and perform fit-up/welding as 5/18/15 2014-207 necessary to support re-aligning the pipe and fittings on KJ148HBC-8" to better align the Garlock coupling to within allowable tolerance.
3 Containment 3Cooler Replace 12 cooling coils with new coils and 5/19/15 2014-096 SGN01A replace all the cooling coil mounting bolts and lock nuts with new material.
3 Containment 3Cooler Replace 12 cooling coils with new coils and 5/19/15 2014-097 SGN01 B replace all the cooling coil mounting bolts and lock nuts with new material.
Containment 3Cooler Replace 12 cooling coils with new coils and 5/19/15 2014-098 replace all the cooling coil mounting bolts and SGN01C lock nuts with new material.
3 Continent Replace 12 cooling coils with new coils and 5/19/15 2014-122 Cooler replace all the cooling coil mounting bolts and SGN01 D lock nuts with new material.
2 Residual Heat Replaced damaged pump diffuser, seal 5/12/15 201 5-032 Removal Pump housing, and tack weld bearing retainer cap PEJ~lA screws.
3 Spent Fuel Installed welded tube plugs in the inlet and 6/17/15 2014-003 Cooling HX outlet for 3 tubes 1-1, 4-1, and 5-1. The outlet of tube 1-1 had a 10' tube stake welded to the EECO1B inner end of the plug and installed in the tube.
3 ALV0002 Replaced valve with a like-for-like valve due to 2/3/14 2012-044 8" Ceck alve ID pitting and the valve dimensional criteria was out of tolerance 3 ESW Piping Installed a 2" encapsulation over degraded 2/19/14 201 3-104 area on spool EF03-S009/142 due to ID EG205HBC-24 ptig 3EEC01A Installed welded tube plugs in inlet and outlet 8/5/13 201 3-1 09 tube 1-1. Installed 10' tube stake welded to Fuel Pool Cooling the plug and installed outlet tube 1-1.
3PEG01A Performed base metal repairs of eroded areas 9/23/13 2013-219
_____ CCWPump on the inside of pump casing.
OAR-i1 13-P3-RF-20 Page 3 of 6
Code Item Description of Work Date Repair/Replacement Class Description Completed Plan Number (Note 1) 3 EF1 29HBC-24 Installed 6" encapsulation on minimum wall 7/1/13 2013-295 violation indications M-1 3EF04-EF1 29HBC-24-BAUX-04A and M-1 3EF04-EF1 29HBC24-B001A on line EF129HBC-24 3 EFHV0092 Replaced 3" Motor Operated Gate Valve due 4/14/14 2014-042 to over torqueing of the operator.
3 A Emerg Diesel Realigned piping to within specifications for 6/10/15 2014-058 EKJOA HX flex coupling.
3 ESW Pre Lube Replaced the Pre-Lube Storage Tank with a 6/17/15 2014-050 new Design as approved by CCP 14727.
TEF~lA Replace a portion of spools EF173HBC-2, EF184HBC-2 and EF192HBC-2. Tank replaced due to ID Pitting.
3 A Emerg Diesel Realigned piping to within specifications for 3/21/15 2014-060 KJO49BC..8 flex coupling between EKJ04A and EFV0053.
3 ESW Piping Installed 2" encapsulation over minimum wall 6/25/2015 2014-092 defect on piping spool EF04-S006/1 33 due to E~l 92BC-24 ID pitting.
3 CCW Cooling Performed base metal repairs of erode areas 6/10/15 2014-1 54 PEGOID in the upper and lower pump casing.
3 EG03R0261 41 Replaced existing sway strut with new from 6/17/15 2012-087 warehouse stock.
2 EGV0204 Performed base metal repair on three worn 5/19/15 2015-057 areas on the valve body and weld build-up on worn area on portion the travel stop of disc arm to return the valve to full compliance with the original design.
1RBB01 Installed canopy seal weld clamp on capped 6/15/15 2015-044 latch housing penetration No. 20.
3 EF1 41 HBC-4 Replaced 1-EF-14-S-008/341 spool for min 5/19/15 2015-035 wall violation (like-for-like).
1 PSA-1/2 S/N Replaced damaged housing and insert 1/21/15 2014-1 92 15022 assembly on PSA-1/2 S/N 15022 snubber with new replacement part.
I PSA-1/4 S/N Replaced damaged housing and insert 1/21/15 2014-1 93 16449 assembly on PSA-1/4 S/N 16449 snubber with new replacement part.
OAR-I I3-P3-RF-20 Page 4 of 6
Code Item Description of Work Date Repair/Replacement Class Description Completed Plan Number (Note 1) 1 PSA-1/4 S/N Replaced damaged torque carrier and shaft 1/21/15 2014-194 24289 assembly on PSA-1/4 S/N 24289 snubber with new replacement part.
1 PSA-i00 S/N Replaced damaged telescoping cylinder on 1/21/15 2014-180 1390 PSA-1 00 S/N 1390 snubber with new replacement part.
I PSA-3 S/N 8435 Replaced damaged bearing retainer nut on 1/21/15 2014-1 81 PSA-3 S/N 8435 snubber with new replacement part.
3 EF04-S006/131 Installed 2" encapsulation over degraded area 6/25/15 2014-092 Ml13EF04-EF1 29HBC24-BGWT-84-02 on pipe spool EF04-S006/1 33.
3SGN01C Removed cooling coil on SGN01C from 5/28/14 2014-063 service due to leak. The inlet and outlet flanges from the cooling coil were cut and blind flanges were installed.
3SGN01B Removed cooling coil on SGN01B from 6/18/14 2014-064 service due to leak. The inlet and outlet flanges from the cooling coil were cut and blind flanges were installed.
1 PSA-35 S/N Replaced damaged telescoping cylinder on 6/17/15 2014-204 11690 PSA-35, S/N 11690, snubber with new replacement part.
3 SGN01D Removed leaking coil S/N 906-897-D4 and 5/28/14 2014-043 install S/N 906-897-D2 replacement cooling coil in top north bank in SGN01 D cooler.
3 EF06C0551 25 Replaced existing Corner Lada Strut (item 3 6/29/15 201 3-059 on design drawing M-O6EF06C055125) with new ITT Grinnell (figure 211 )
3 EG210HBC-24 Replaced all of spool EF04-S009/141 on line 6/23/15 2014-106 EG2I0HBC-24 in accordance with CCP 14266.
BECHTEL POWER CORPORATION 3 EFO54HBC-8 replaced EF02-S029/124, EF02-S030/124 62/0421-6 and a portion of EF02-S031/124 on line EF-054HBC-8.
Note 1: The date completed is the date the Form NIS-2A was certified.
OAR-I 13-P3-RF-20 Page 5 of 6
ATTACHMENT 1 Code Cases used:
N-460 N-513-2 N-532-4 N-533-1 N-552 N-566-2 N-616 N-623 N-624 N-639 N-652 N-658 N-685 N-686 N-695 N-700 N-706 OAR-i 13-P3-RF-20 Page 6 of 6