ML093170375

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IR 05000387-09-004, 05000388-09-004, 07/01/2009 - 09/30/2009; Susquehanna Steam Electric Station, Units 1 and 2; Fire Protection, Licensed Operator Requalification Program, Maintenance Effectiveness, ALARA Planning and Controls
ML093170375
Person / Time
Site: Susquehanna  Talen Energy icon.png
Issue date: 11/13/2009
From: David Lew
Division Reactor Projects I
To: Rausch T
Susquehanna
KROHN P, RI/DRP/PB4/610-337-5120
References
EA-09-248 IR-09-004
Download: ML093170375 (47)


See also: IR 05000387/2009004

Text

UNITED NUCLEAR REGULATORY

REGION 475 ALLENDALE KING OF PRUSSIA, PA

November 13, 2009 EA-09-248

Mr. Timothy S. Rausch Senior Vice President

and Chief Nuclear Officer PPL Susquehanna, LLC 769 Salem Boulevard, NUCSB3 Berwick, PA 18603

SUSQUEHANNA

STEAM ELECTRIC STATION -NRC INTEGRATED

INSPECTION

REPORT 05000387/2009004

AND 05000388/2009004

Dear Mr. Rausch: On SeptElmber

30, 2009, the U. S. Nuclear Regulatory

Commission (NRC) completed

an inspection

at your Susquehanna

Steam Electric Station Units 1 and 2. The enclosed integrated

inspection

report presents the inspection

results, which were discussed

with you and other members of your staff during a preliminary

exit meeting on October 9, 2009. This inspection

examined activities

completed

under your license as they relate to safety and compliance

with the Commission's

rules and regulations

and with the conditions

of your license. The inspectors

reviewed selected procedures

and records, observed activities, and interviewed

personnel.

Based on the results of this inspection, two examples of an apparent violation (A V) were identified, involving

PPL Susquehanna, LLC (PPL) failing to ensure that individual

license holders, on shift in the capacity of senior reactor operators (SROs), met the medical prereqUisites

required for holding a license prior to performing

the duties of a licensed operator as required by 10 CFR 55.3. In one occasion in August 2009, an SRO failed a medical examination

which identified

a disqualifying

condition, in that, the examination

identified

that the SRO's vision did not meet the health requirements

stated in ANSI/ANS 3.4-1983, Section 5.4.5, "Eyes." However, he performed

the function of an SRO during three watches with a license that was not appropriately

conditioned

to require that corrective

lenses be worn. In the second occasion, a different

SRO performed

licensed operator duties 52 times between April 1, 2009, and July 22, 2009, after the deadline for his biennial medical examination

had passed. The medical examination

may have identified

an issue with the SRO's medical condition

and general health that would have disqualified

him from being authorized

by a license. This app,arent

violation

is being considered

for escalated

enforcement

action in accordance

with the NRC Enforcement

Policy. The current Enforcement

Policy is included on the NRC's Web site at (http://www.nre.gov/about-nrciregulatorv/enforcementienforce-pol.html).

T. Rausch 2 Upon discovery, PPL removed both individuals

from watchstanding

duties pending follow-up

medical evaluations

and, in the August 2009 example involving

the SRO who failed his vision examination

resulting

in a disqualifying

condition, PPL requested

a conditional

NRC license to address the disqualifying

medical condition.

For the July 2009 example, the SRO passed his biennial medical examination

when administered.

Both issues have been entered into PPL's corrective

action program. See Section 1 R11 of the attached report for additional

details. In addition, since you identified

the violation, and based on our understanding

of your corrective

actions, a civil penalty may not be warranted

in accordance

with Section VI.C.2 of the Enforcement

Policy. The NRC believes we have enough information

to make a final decision on the matter. Before the NRC makes its enforcement

decision, we provided you an opportunity

to either: (1) respond to the apparent violation

addressed

in this inspection

report within 30 days of the date of this letter or, (2) request a predecisional

enforcement

conference.

On November 9, 2009, I contacted

Mr. Jeff Helsel, Susquehanna

Plant Manager, and members of your staff and informed them of this opportunity.

On November 10, 2009, Michael Crowthers, Susquehanna

Regulatory

Assurance

Manager, informed my staff that you elected to provide a written response.

Your written response should be clearly marked as a "Response

to an Apparent Violation

in Inspection

Report 0500038"712009004

AND 05000388/2009004;

EA-09-248" and should include for each example of the AV: (1) the reason for the AV, or, if contested, the basis for disputing

the AV; (2) the corrective

steps that have been taken and the results achieved;

(3) the corrective

steps that will be taken to avoid further violations;

and (4) the date when

full compliance

will be achieved.

Your response may reference

or include previously

docketed correspondence, if the correspondence

adequately

addresses

the required response.

If an adequate response is not received within the time specified

or an extension

of time has not been granted by the NRC, the NRC will proceed with its enforcement

decision.

In addition, please be advised that the number of violations

and characterization

of the AV described

in the enclosed inspection

report may change as a result of further NRC review. You will be advised by separate correspondence

of the results of our deliberations

on this matter. In addition, this report documents

two NRC-identified

findings and one self-revealing

finding of very low safety significance (Green). Two of these findings were determined

to involve a violation

of NRC requirements.

Additionally, one licensee-identified

violation, which was determined

to be of very low safety significance, is listed in this report. However, because of the very low safety significance

and because they are entered into your corrective

action program (CAP), the NRC is treating these findings as non-cited

violations (NCVs), consistent

with Section VI.A.1 of the NRC Enforcement

Policy. If you contest any NCV in this report, you should provide a response within 30 days of the date of this inspection

report, with the basis for your denial, to the Nuclear Regulatory

Commission, ATTN.: Document Control Desk, Washington, D.C. 20555-0001;

with copies to the Regional Administrator

Region I; the Director, Office of Enforcement, United States NRC, Washington, D.C. 20555-0001;

and the NRC Resident Inspector

at the Susquehanna

Steam Electric Station. In addition, if you disagree with the characterization

of the cross cutting aspect of any finding in this report, you should provide a response within 30 days of the date of this inspection

report, with the basis for your disagreement, to the Regional Administrator, Region I, and the NRC Resident Inspector

at the

T. Rausch 3 Susquehanna

Steam Electric Station. The information

you provide will be considered

in accordance

with Inspection

Manual Chapter 0305. In accordance

with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any), will be available

electronically

for public inspection

in the !\IRC Public Document Room or from the Publicly Available

Records (PARS) component

of the NRC's document system (ADAMS). ADAMS is accessible

from the NRC Web site at http://www.nrc.qov/reading-rm/adams.html(the

Public Electronic

Reading Room). Sincerely, IRA! David C. Lew, Director Division of Reactor Projects Docket Nos. 50-387; 50-388 License Nos. NPF-14, NPF-22 Enclosures:

Inspection

Report 05000387/2009004

and 05000388/2009004

Attachment:

Supplemental

Information

cc w/encl: Distribution

via ListServ

T. 4 Susquehanna

Steam Electric Station. The information

you provide will be considered accordance

with Inspection

Manual Chapter In accordance

with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any), will be available

electronically

for public inspection

in the NRC Public Document Room or from the Publicly Available

Records (PARS) component

of the NRC's document system (ADAMS). ADAMS is accessible

from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html(the

Public Electronic

Reading Room). Sincerely, IRA! David C. Lew, Director Division of Reactor Projects Docket Nos. 50-387; 50-388 License Nos. NPF-14, NPF-22

Inspection

Report 05000387/2009004

and 05000388/2009004

Attachment:

Supplemental

Information

cc Distribution

via ListServ Distribution

w/encl: (via E-mail) S. Collins, (R10RAMAIL

Resource)

M. Dapas, (R10RAMAIL

Resource)

D. Lew, (R1 DRPMAIL Resource)

J. Clifford, (R1 DRPAMAIL Resource)

P. Krohn, DRP D. Holody OE (R10RAMAIL

Resource)

R Fuhrmeister, DRP A. Rosebrook, DRP E. Torres, DRP J. Bream, DRP F. Jaxheimer, DRP, SRI P. Finney, DRP, RI S. Farrell, DRP, OA L. Trocine, RI OEDO RidsNrrPMPeachBottom

Resource RidsNrrDorlLpl1-2

Resource ML093170375

SUNSI Review Complete:

AAR (Reviewer's

Initials)

DOCUMENT NAME: G:\DRP\BRANCH4\lnspection

Reports\Susquehanna\SQ

3rd Qtr 2009\SUS2009

_004 _g.doc After declaring

this document "An Official Agency Record" it will be released to the Public. To receive a copy of this document.

indicate in the box: "C":: Copy without attachment/enclosure "E";; Copy with attachmenUenciosure

liN" No copy OFFICE RIIDRP I RI/DRP I R1/0E I R1/DRP I NAME ARosebrookl

PKrohnl DHoiody/AED

for DLew lOATE 11/12/09 11/12/09 11112109 11/12/09 OFFICIAL RECORD COPY

Docket No: License No: Report No: Licensee:

Facility:

Location:

Dates: Inspectors:

Reviewed By: Approved By: U.S NUCLEAR REGULATORY

COMMISSION

REGION I 50-387, 50-388 NPF-14, NPF-22 05000387/2009004

and 05000388/2009004

PPL Susquehanna, LLC Susquehanna

Steam Electric Station, Units 1 and 2 Berwick, Pennsylvania

July 1, 2009 through September

30, 2009 F. Jaxheimer, Senior Resident Inspector

P. Finney, Resident Inspector

G. Meyer, Senior Reactor Inspector

S. Chaudhary, Reactor Inspector

J. Furia, Senior Health Physicist

A. Rosebrook, Senior Project Engineer O. Masnyk-Bailey, Health Physicist

S. Hammann, Health Physicist

J. Nicholson, Health Physicist

Paul G. Krohn, Chief Projects Branch 4 David C. Lew, Director Division of Reactor Projects Enclosure

TABLE OF

SUMMARY OF FINDINGS .........................................................................................................REPORT DETAILS .....................................................................................................................1. REA,CTOR SAFETy ...........................................................................................................1 R04 Equipment

Alignment

..............................................................................................1 R05 Fire Protection

.........................................................................................................1 R06 Flood Protection

Measures ......................................................................................1 R07 Heat Sink Performance

...........................................................................................1 R11 Licensed Operator Requalification

Program .......................................................... 1R12 Maintenance

Effectiveness

.................................................................................... 1 R 13 Maintenance

Risk Assessments

and Emergent Work Control ............................... 1 R 15 Operability

Evaluations

.......................................................................................... 1 R 18 Plant Modifications

................................................................................................ 1 R 19 Post-Maintenance

Testing .....................................................................................1 R22 Surveillance

Testing ..............................................................................................1 EP6 Drill Evaluation

......................................................................................................2. RADIATION

SAFETY .......................................................................................................20S 1 Access Control to Radiologically

Significant

Areas ................................................ 20S2 ALARA Planning and Controls ...............................................................................20S3 Radiation

Monitoring

Instrumentation

.................................................................... 4. OTHER ACTiViTIES

.........................................................................................................40A 1 Performance

Indicator

Verification

.........................................................................40A2 Identification

and Resolution

of Problems .............................................................. 40A5 Other Activities

......................................................................................................40A6 Meetings, Including

Exit. ........................................................................................40A7 Licensee-Identified

Violations

................................................................................ ATTACHMENT:

SUPPLEMENTAL

INFORMATION

................................................................ SUPPLE.MENTAL

INFORMATION

......................................................................................... KEY POINTS OF CONTACT .................................................................................................. LIST OF ITEMS OPENED, CLOSED, AND DiSCUSSED

....................................................... LIST OF DOCUMENTS

REVIEWED ...................................................................................... LIST OF ACRONYMS .......................................................................................................... Enclosure

SUMMARY OF

IR 05000387/2009004,05000388/2009004,07/01/2009

-09/30/2009;

Susquehanna

Steam Electric Station, Units 1 and 2; Fire Protection, Licensed Operator Requalification

Program, Maintenance

Effectiveness, ALARA Planning and Controls.

The report covered a 3-month period of inspection

by resident inspectors

and announced

inspections

by regional reactor inspectors.

Two Green non-cited

violations (NCVs), and one Green finding were identified.

In addition, one apparent violation (AV) item being considered

for escalated

enforcement

action in accordance

with the NRC Enforcement

Policy. The current Enforcement

Policy is included on the NRC's Web site at (http://wvvw.nrc.gov/about-nrc!regulatory/enforcementlenforce-pol.html

). The significance

of most findings is indicated

by their color (Green, White, Yellow, or Red) using Inspection

Manual Chapter (IMC) 0609, "Significance

Determination

Process" (SOP). Cross-cutting

aspects associated

with findings are determined

using IMC 0305, "Operating

Reactor Assessment

Program," dated August 2009. Findings for which the SOP does not apply may be Green or be assigned a severity level after NRC management

review. The NRC's program for overseeing

the safe operation

of commercial

nuclear power reactors is described

in NUREG-1649, "Reactor Oversight

Process," Revision 4, dated December 2006. A. NRC-Identified

and Self-Revealing

Findings Cornerstone:

Mitigating

Systems Green. The inspectors

identified

a Green NCV of the Susquehanna, Unit 2 Operating

License Condition

2.C.(3), Fire Protection

for failure to administratively

control combustible

loading in an area on the 686' elevation

of the control structure.

As a result, a normally locked storage area was discovered

to contain numerous combustibles

without deSignated

detection, suppression, or a pre-fire plan. This issue was placed in PPL's corrective action

program (CAP) and immediate

corrective

actions included the removal of some of the combustible

materials

and the assignment

of hourly fire watches. The finding was more than minor because it was associated

with the external factors attribute (fire) of the Mitigating

Systems cornerstone

objective

to ensure the availability, reliability, and capability

of systems that respond to initiating

events to prevent undesirable

consequences.

Specifically, PPL did not ensure that plant procedures

controlled

the use and storage of combustible

materials

and that a combustible

loading analysis was maintained

for a locked storage area fire zone in the control structure.

The inspectors

assessed this finding in accordance

with IMC 0609, Appendix F, "Fire Protection

Significance

Determination

Process", and determined

the finding to be of very low safety significance (Green) because the fire barrier between the safety-related

equipment

in the lower relay room and this storage area was being properly maintained

and found in good physical condition.

The finding was determined

to have a cutting aspect in the area of Problem Identification

and Resolution, Corrective

Action Program, because PPL did not implement

a CAP with a low threshold

for identifying

issues P.1(a).

Specifically, PPL had reasonable

opportunities

to identify the combustible

loading issue on multiple occasions

during access of the storage room. (Section 'I R05) Enclosure

AV... PPL identified

two examples of an apparent violation (AV), involving

PPL Susquehanna, LLC (PPL) failing to ensure that individual

license holders, on shift in the capacity of senior reactor operators (SROs), met the medical prerequisites

required for holding a license prior to performing

the duties of a licensed operator as required by 10 CFR 55.3. In one occasion in August 2009, an SRO failed a medical examination

which identified

a disqualifying

condition, in that, the examination

identified

that the SRO's vision did not meet the health requirements

stated in ANSI/ANS 3.4-1983, Section 5.4.5, "Eyes." However, he performed

the function of an SRO during three watches with a license that was not appropriately

conditioned

to require that corrective

lenses be worn. In the second occasion, a different

SRO performed

licensed operator duties 52 times between April 1, 2009, and July 22, 2009, after the deadline for his biennial medical examination

had passed. The medical examination

may have identified

an issue with the SRO's medical condition

and general health that would have disqualified

him from being authorized

by a license. Upon discovery, PPL removed both individuals

from watchstanding

duties pending follow-up

medical evaluations

and, in the case involving

the SRO whose failed medical examination

resulted in a disqualifying

condition, PPL requested

a conditional

NRC license to address the disqualifying

medical condition.

Both issues have been entered into PPL's corrective

action program. Each example was evaluated

independently

using the traditional

enforcement

process bf:lcause

the failure to determine

an operator's

medical condition

and general health has the potential

to impact or impede the regulatory

process. Specifically, medical certification

and conditional

licensing

are used by the NRC to ensure health conditions

wi" not adversely

affect operator duties or performance. The

finding was determined

to have a cross-cutting

aspect in the area of Problem Identification

and Resolution, Operating

Experience, because PPL did not systematically

collect, evaluate, and communicate

relevant external operating

experience

P.2(a).

Specifically, PPL failed to evaluate NRC Information

Notice 2004-20 for medical examination

issue applicability

in accordance

with their operating

experience

review program as evidenced

by the 2008 SL-IV NCV (NRC IR 50-387 & 50-388 2008302-01), for an initial licensed operator application

submitted

to the NRC with a disqualifying

medical condition, as well as these two events in July and August of 2009. (Section 1 R11.2) Green. The inspectors

identified

a Green NCV of 10 CFR Part 50, Appendix B, Criterion

XVI, "Corrective

Action," in that PPL did not implement

timely corrective

actions to preclude repetition

of a significant

condition

adverse to quality. Specifically, actions taken to address causes of the Unit 1 high pressure coolant injection (HPCI) stop valve failure to close in 2006 did not prevent the same HPCI stop valve from failing to close on August 18, 2009. In both cases, the stop valve failure to close rendered this single train HPCI system inoperable

as it was unable to meet the 30 second injection

response time as described

in the design basis. Corrective

maintenance

was performed

on the valve and the issue was entered into PPL's CAP. The finding is more than minor because it adversely

affected the performance

attribute

of the Mitigating

Systems cornerstone

objective, to ensure the availability, reliability, and capability

of equipment

that respond to initiating

events to prevent undesirable

consequences.

Specifically, a full closed stop valve indication

resets the HPCI ramp generator

via a lower limit switch. Without this reset, the governor is unprepared

to restart the turbine from an idle state during a designed basis event. The inspectors

assessed this finding in accordance

with IMC 0609, Attachment

4, "Phase 1 Initial Screening

and Characterization

of Findings" and determined

the finding to be of very low Enclosure

safety significance

because it did not result in an actual loss of safety function for greater than the Technical

Specification

allowed outage time. The finding was determined

to have a cross-cutting

aspect in the area of Problem Identification

and Resolution, Corrective

Action Program, because PPL did not take appropriate

corrective

actions to address safety issues in a timely manner, commensurate

with their safety significance

and complexity

[P .1 (d)]. Specifically, PPL did not appropriately

implement

corrective

actions following

the 2006 failure of the HPCI stop valve. (Section 1 R12) Cornerstone:

Occupational

Radiation

Safety Green. A self-revealing, Green finding was identified

that involved inadequate

work planning relative to the in-vessel

visual inspection!

inservice

inspection (lWIIISI)

of the reactor vessel that resulted in additional

unplanned

collective

exposure contrary to low-as-is-reasonably-achievable (ALARA) controls.

Specifically, the utilization

of inexperienced

workers to perform the various tasks involved in the IWIlISI activity resulted in the additional

collective

exposure to perform this routine task. This finding was entered into PPL's Correction

Action Program for resolution.

This finding is more than minor because it resulted in unplanned, unintended

collective

exposure that was greater than 50 percent above the intended collective

exposure and greater than 5 person-rem.

Additionally, the performance

deficiency

adversely

affected the radiation

protection

cornerstone

objective.

The inspectors

assessed the finding in accordance

with IMC 0609, Appendix C, "Occupational

Radiation

Safety Significance

Determination

Process," and determined

that the finding was of very low safety significance (Green) because the finding was due to ALARA work control planning and the 3-year rolling average collective

exposure at Susquehanna

was less than 240 person-rem

(107 person-rem

for 2005-2007).

This finding was determined

to have a cross-cutting

aspect in the area of Human Performance, Resources, because PPL did not utilize sufficiently

qualified

personnel

to assure occupational

radiation

safety requirements

were met H.2{b).

Specifically, PPL's use of inexperienced

contract workers resulted in additional

collective

exposure that could have been avoided. (Section 20S2) B. Licensee Identified

Violations

A violation

of very low safety significance.

which was identified

by PPL. has been reviewed by the inspectors.

Corrective

actions taken or planned by PPL have been entered into PPL's CAP. This violation

and corrective

action tracking numbers are listed in Section 40A7 of this report. Enclosure

.1 REPORT Summary of Plant Status Susquehanna

Steam Electric Station (SSES) Unit 1 began the inspection

period at the authorized

licensed power level of 94.4 percent rated thermal power (RTP). On September

4, 2009, Unit 1 was reduced to 70 percent over 26 hours3.009259e-4 days <br />0.00722 hours <br />4.298942e-5 weeks <br />9.893e-6 months <br /> in support of a control rod sequence exchangEl

and pattern adjustment.

Unit 1 remained at 94.4 percent RTP for the remainder

of the inspection

period. SSES Unit 2 began the inspection

period at the authorized

licensed power level of 94.4 percent RTP. On September

12,2009, Unit 2 was reduced to 58 percent over 26 hours3.009259e-4 days <br />0.00722 hours <br />4.298942e-5 weeks <br />9.893e-6 months <br /> in support of a control rod sequence exchange and pattern adjustment.

Unit 2 remained at 94.4 percent RTP for the remainder

of the inspection

period. Note: The licensed RTP for both units is 3952 megawatts

thermal. The Extended Power Uprate (EPU) License Amendment

for SSES was approved in January 30,2008, and was implemented

for both units in accordance

with the issued license conditions.

For the current inspection

period, the authorized

power level for both units is 94.4 percent of the EPU licensed power limit. REACTOR SAFETY Cornerstones:

Initiating

Events, Mitigating

Systems, and 8arrier Integrity

1 Equipment

Alignment

Partial Walkdown (71111.04 -3 Samples) a. Inspection

Scope The inspectors

performed

partial walkdowns

to verify system and component

alignment

and to identify any discrepancies

that would impact system operability.

The inspectors

verified that selected portions of redundant

or backup systems or trains were available

while certain system components

were out-of-service.

The inspectors

reviewed selected valve positions, electrical

power availability, and the general condition

of major system components.

Documents

reviewed are listed in the Attachment.

The walkdowns

included the following

systems: Unit 1, 18 residual heat removal (RHR) components

and instrumentation

with focus on behavior during pressurization

and venting; Plant discharge

line (blow down) and river water make-up system parameters

and lineup during investigation

of groundwater

issue described

by CR 1167146; and "An and "En emergency

diesel generators (EDGs) when "En EDG substituted

for "8" EDG. b. Findings No findings of significance

were identified.

Enclosure

.2 Complete Walkdown (71111.04S -1 Sample) a. Inspection

Scope The inspectors

performed

a detailed review of the alignment

and condition

of the station nitrogen system and the Unit 2 containment

instrument

gas system. The inspectors

reviewed operating

procedures, checkoff lists, and system piping and instrumentation

drawings.

Walkdowns

of accessible

portions of the systems were performed

to verify components

were in their correct positions

and to assess the material condition

of systems and components.

The inspectors

evaluated

ongoing maintenance

and outstanding

Condition

Reports (CR) associated

with both systems to determine

the effect on system health and reliability.

The inspectors

verified proper system alignment

and looked at system operating parameters.

Documents

reviewed are listed in the Attachment.

The walkdown included

the following

system and its interconnection: Unit 2, Nitrogen and Primary Containment

Instrument

Gas. b Findings No findings of significance

were identified. 1 Fire Protection

(71111.050 -5 Samples) Fire Protection

-Tours a. Inspection

Scope The inspectors

reviewed PPL's fire protection

program to evaluate the specified

fire protection

deSign features, fire area boundaries, and combustible

loading requirements

for selected areas. The inspectors

walked down those areas to assess PPL's control of transient

combustible

material and ignition sources, fire detection

and suppression

capabilities, fire barriers, and any related compensatory

measures to assess PPL's fire protection

program in those areas. Documents

reviewed are listed in the Attachment.

The inspected

areas included: Unit 1, battery rooms, fire zones 0-28 B-1 (11) and 0-28 I thru N; Unit 1, containment

access area (1-401); Security control center, fire zone 0-83, FP-013-360; Control structure

charcoal filter area and operations

storage area on elevation

687', FP-013-135;

and Central access control area and chemistry

laboratory, elevation

676', 134. b. Findings Introduction:

The inspectors

identified

that PPL was not administratively

controlling

combustible

loading in an area on the 686' elevation

of the control structure

as specifically

required by the Susquehanna

Fire Protection

Program and specifically

described

as a provision

of the Fire Protection

Program Report (FPPR). This finding Enclosure

was determined

to be of very low safety significance (Green) and an NCV of the SSES Unit 2 Operating

License Condition

2.C(3), Fire Protection.

Description:

During a fire walkdown inspection

in the control structure, the resident inspectors

identified

that an operations

department

space, a normally locked storage area on 686' elevation, contained

numerous combustibles.

Most items stored in the area were found on open shelves or stacked on the floor. The accumulation

of combustibles

included (but was not limited to) wood, plastic, cardboard

boxes, old paper records, rubber drain hoses, radio equipment, refueling

support furniture, and labeling supplies.

Inspectors

immediately

asked operations

staff if this room was part of any fire pre-plan (fire fighting guideline/procedure).

The room was not incorporated

in any of the site fire pre-plans

and inspectors

did not locate any combustible

storage permits. When inspectors

could not verify the area was being controlled

by the design control process as a combustible

storage area and could not verify that PPL was procedurally

controlling

the use and storage of combustible

materials

in this area, the issue was brought to PPL management's

attention.

PPL took immediate

action to dispatch the fire protection

engineer (FPE) and field unit supervisor

to the area. An hourly fire watch was started for the area and some of the combustibles

were promptly removed from the room. The operations

shift manager determined

that the area was overcrowded

with materials

that were no longer needed. Longer term correction

actions are planned and the issue is

tracked by CR 1179995. As part of the evaluation

of this performance

issue, inspectors

also completed

additional

walkdowns

and drawing reviews which revealed that the operations

department

storage area was actually located directly below the following

rooms on the 698' elevation

of the control structure: the

computer maintenance

room, the uninterrupted

power supply computer room, Corridor C-200, and the Unit-2 lower relay room. Inspectors

reviewed

drawings, the FPPR and held a discussion

with the site FPE, to verify that there was no automatic

detection, no automatic

suppression, and no fire pre-plan for this storage area. Analysis:

The inspectors

determined

that this finding was more than minor because it was associated

with the external factors attribute (fire) of the mitigating

systems cornerstone

objective

to ensure the availability, reliability, and capability

of systems that respond to initiating

events to prevent undesirable

consequences (Le., core damage). Specifically, PPL did not ensure that fire combustible

storage was procedurally

controlled

in the control structure.

Fire combustibles

accumulated

in an area directly b,elow the Unit 2 relay room and three other separated

rooms. This storage area did not have any fire suppression

or detection

capability.

The inspectors

assessed this finding in accordance

with IMC 0609, Appendix F, "Fire Protection

Significance

Determination

Process." This finding was determined

to be of very low safety significance (Green) in Phase 1 of the SDP because it was assigned a low degradation

rating. A low degradation

rating was assigned because the fire barrier between the safety-related

equipment

in the lower relay room and this storage area was being properly maintained

and found in good physical condition.

The finding was determined

have a cross-cutting

aspect in the area of Problem Identification

and Resolution, Corrective

Action Program, because PPL did not implement

a CAP with a low threshold

for identifying

issues [P.1 (a)]. Specifically, PPL Enclosure

had reasonable

opportunities

to identify the combustible

loading issue on multiple occasions

during access of the storage room. Enforcement:

The Susquehanna

Unit 2 Operating

License Condition

2.C.(3), requires that PPL implement

and maintain in effect all provisions

of the Fire Protection

Program as described

in the FPPR. FPPR section 1.4 requires that plant procedures

control the use and storage of combustible

materials

and section 6.0 also requires that the combustible

loading analysis was maintained through

the design control process. Contrary to these requirements, prior to September

2009 PPL did not procedurally

control the use and storage of combustible

materials

on the 686' elevation

of the control structure

and did not evaluate changes to combustible

storage in this area through the

control process. Because the finding is of very low safety significance

and has been entered into PPL's CAP (CR 1179995), this violation

is being treated as a Cited Violation (NCV), consistent

with Section VI.A of the NRC Enforcement

Policy. (NCV 05000388/2009004-01, Failure to Implement

and Maintain the Fire Protection

Program with Respect to the Use and Storage of Combustibles

in the Control Structure) 1 Fiood Protection

Measures (71111.06

-1 Sample) Underground

Cables a. Inspection

Scope The inspectors

reviewed documents, interviewed

plant personnel, and entered four underground

vaults to evaluate the conditions

of risk-significant

cables. The inspection

focus included a visual inspection

of cable integrity.

Additionally, the material condition

o'f support structures

and credited components

such as watertight

plugs, floor drains, flood detection

equipment, and alarms were also assessed to determine

whether the components

were capable of performing

their intended function.

Some dewatering

devices were observed in operation.

Documents

reviewed are listed in the Attachment.

The following

risk significant

area was reviewed: Engineered

Safeguards

Service Water pump house and spray pond vault inspections

VA006, VA007, VA011, and VA012. b. Findings No findings of significance

were identified.

1 Heat Sink Performance

(71111.07T -3 Samples) Triennial

Heat Sink a. Inspection

Scope Based on safety significance

and prior inspection

history, the inspectors

selected the following

heat exchangers

to evaluate PPL's means (inspection, cleaning, maintenance, and performance

monitoring)

of ensuring adequate heat sink performance. Unit 1 A RHR heat exchanger;

Enclosure

10 'A' Emergency

diesel generator

heat

1) Intercooler

heat

2) Jacket water cooler; 3) Lubricating

oil 'E' Emergency

diesel generator

heat

1) Intercooler

heat

2) Jacket water cooler; 3) Lubricating

oil The inspectors

assessed the external condition

of the above heat exchangers

in the field, reviewed the eddy current, surveillance

test and inspection

results, and reviewed the applicable

system health reports since the last inspection

to confirm that results were acceptable

and that design basis assumptions

for flow rate, plugged tube percentage, and heat transfer capability

had been met. The inspectors

discussed

piping corrosion, and heat exchanger

practices, including

the specifications

and procedures

for heat exchanger

maintenance, and consistency

with the Generic Letter 89-13 requirements

with cognizant, system engineers, and chemistry

personnel.

The inspectors

reviewed applicable

corrective

action program documents

to confirm that identified

problems and d,egraded

conditions

had been resolved properly.

In addition to the inspections

of heat exchangers

in the RHR and EDG systems, the inspectors

visually examined equipment, slope protection

and water level in the spray pond, and the apparent condition

of primary and support equipment

in the intake structure.

The inspectors

assessed the condition

of the spray pond (ultimate

heat sink) and the pump house, and reviewed the August 2009 inspection/evaluation

of spray pond sediment depth. The review included discussions

with the RHR service water system engineer, a walk-down

of the spray pond and pump house, and discussions

with cl1emistry

personnel

and the emergency

service water (ESW) system engineer.

The chemical treatment

programs for the spray pond (ESW ultimate heat sink) and the cooling tower basin (service water heat sink) were reviewed to verify that potential

bio-fouling

mechanisms

were being addressed, including

on-going treatment

and monitoring

as specified

in the chemistry

manual. The inspectors

noted that the SSES results were aided by the ability to chemically

control their ultimate heat sink, the extensive

use of stainless

steel AL-6XN in tubing, and the experience

of involved engineering, testing, and chemistry

personnel.

Documents

reviewed are listed in the Attachment.

b. Findings No findings of significance

were identified.

Enclosure

.1 1Licensed Operator Requalification

Program (71111.11 Q -2 Sample) Resident Inspector

Quarterly

Review a. Inspection

Scope On August 10, 2009, the inspectors

observed as-found licensed operator simulator

performance.

The inspectors

compared their observations

to Technical

Specifications (TSs), emergency

plan implementation, and the use of system operating

procedures.

Tlhe inspectors

also evaluated

PPL's critique of the operators'

performance

to identify discrepancies

and deficiencies

in operator training.

Documents

reviewed are listed in the Attachment.

The following

training was observed: Anticipated

transient

without scram, reactor pressure vessel power and level control, and event declaration.

b. Findings No findings of significance

were identified . . 2 Licensed Operator Medical Review (1 sample) a.. Inspection

Scope The inspectors

reviewed two instances

in July 2009 and August 2009 where PPL had identified

issues with the medical qualification

records for two separate Senior Reactor Operators.

The inspectors

reviewed the medical certification

forms, reviewed the PPL's formal correspondence

with the NRC upon discovery

of the issue to ensure timeliness

requirements

were met, PPL conditional

license request submittal

and reviewed PPL's corrective

actions. b. Findings Introduction:

The licensee identified

two examples of an AVof 10 CFR 55.3, Licensed Requirements, for two cases in which PPL licensed operators

failed to have valid medical examinations

consistent

with their position.

Specifically, one licensed operator performed

duties with an expired biennial medical examination

while another licensed operator performed

duties with a failed visual examination.

In both cases, operators

performed

the function of a senior reactor operator without meeting the medical

for requalification

specified

in 10 CFR 55.21, 10 CFR 55.23 and 10 CFR 55.33. As such both operators

were not qualified

while being assigned to and performing

licensed duties as required by 10 CFR 55.3. Discussion:

During July and August 2009, two instances

were identified

where SSES licensed operators

failed to meet the medical requirements

to maintain their license, and these operators

subsequently

performed

licensed operator duties. ,!;,vent 1: On October 13, 2008, a senior reactor operator (SRO) self-identified

a medical issue that resulted in his disqualification, a medical restriction

entered into a corporate

database and an automatic

update of TMX, (the site's training and qualification

database)

was completed

from the corporate

source. The operator subsequently

Enclosure

completed

a medical follow-up

and was reinstated

on December 12, 2008. While the corporate

database entry could have been deleted upon reinstatement, manual corrections

to TMX were made. When the restriction

was manually updated with a December 12, 2008 date, TMX automatically

and incorrectly

changed the medical examination

due date to October 31, 2010, to reflect a biennial requirement

from the date of the SRO's self-identified

medical issue. In 2004, the NRC issued NUREG-1021, Revision 9, which clarified

the periodicity

of medical examinations.

Appendix F of the NUREG defines biennial as 730 days and allows for an extension

to include the remaining

days in the anniversary

month. For example, the subject SRO had a biennial medical examination

due on March 9, 2009, exactly two years from the previous examination

but the permitted

extension

carried the due date to March 31,2009. During a medical record review on July 22, 2009, PPL discovered

that the SRO had not received a biennial licensed medical examination

by March 31, 2009. The SRO qualifications

for the individual

were immediately

revoked and a physical was scheduled

for July 24, 2009. The operator passed the physical examination

and was subsequently

reinstated

on July 30,2009. Upon review, it was determined

that the SRO stood a total of 52 watches in a TS licensed position without a certifying

medical examination

as outlined in ANSI/ANS-3.4-1983, "Medical Certification

and Monitoring

of Personnel

Requiring

Operator Licenses for Nuclear Power Plants." Upon discovery, PPL placed this issue in their corrective

action program under CR 1166686. Event 2: On August 18, 2009, a PPL health services specialist

determined

that an shift SRO did not pass the corrected

or uncorrected

visual examination

which had been performed

during the previous week. Upon discovery, the SRO was disqualified

for the licensed position and the operator was removed from standing watch. PPL operations

staff promptly initiated

Condition

Report 1173182, which described

the non-compliance

and established

corrective

actions to implement

measures to mitigate the recurrence

of similar conditions.

PPL also implemented

actions to request a conditional

license for this SRO adding a condition

to the operator's

license requiring

corrective

lenses be worn. It was determined

that the licensed operator performed

licensed duties during three scheduled

work shifts which included assuming the role of the refueling

SRO during fuel moves for a dry fuel storage campaign.

This SRO performed

licensed duties even though he had not met the medical condition

and general health prescribed

for licensed operators

at the facility as outlined on NRC Form 396 and required by 10 CFR 55.21. Information

Notice (IN) 2004-20, "Recent Issues Associated

with NRC Medical

Requirements

for Licensed Operators," states, "Given the importance

of the operators'

role in maintaining

reactor safety, the NRC staff becomes concerned

whenever inspection

results, facility audits, and other indicators

suggest that facility medical programs may not be receiving

sufficient

management

oversight

to ensure that the fitness of licensed operators

is being maintained

at the required level." Despite the fact that PPL entered IN 2004-20 into their corrective

action program for operating

experience

evaluation (CRs 625137 and 622658), that evaluation

did not occur. Enclosure

Analysis:

Event 1: The inspectors

determined

that PPL's failure to ensure that the licensed operator received a biennial medical examination

was a performance

deficiency.

This finding was evaluated

using the traditional

enforcement

process because the failure to determine

an operator's

medical condition

and general health has the potential

to impact or impede the regulatory

process. Specifically, there was potential

for license termination

or the issuance of a conditional license

to accommodate

the medical problems.

This operator performed

licensed duties during 52 scheduled

work shifts as an SRO. Tile NRC notes that the operator was actually qualified

the entire time (his follow-up

medical examination

results were satisfactory), he had not developed

any condition

that required a license condition

and there was no actual impact to his requalification;

the fact that the SRO was never the only SRO being credited to met minimum TS manning requirement;

and the fact that the SRO's job performance

was satisfactory

during the period of the expired physical examination, and these factors will be considered

prior to a final severity level determination.

Event 2: The inspectors

determined

that PPL's failure to ensure that the licensed operator received the required vision examination

and passed the required visual before assuming licensed reactor operator duties was a performance

deficiency.

This finding was evaluated

using the traditional

enforcement

process because the failure to determine

an operator's

medical condition

and general health has the potential

to impact or impede the regulatory

process. Specifically, there was a potential

for license termination

or the issuance of a conditional

license to accommodate

for medical problems.

This operator perform licensed duties during three scheduled

work shifts, which included assuming the role of the refueling

SRO during fuel moves for the ongoing dry fuel storage campaign, but he did so with a disqualifying

condition

that would have required his license to be amended. The NRC notes that the Fuel Handling SRO position is a procedurally

required position which was performed

by a qualified

individual;

the SRO had an actual disqualifying

medical condition

which required an amended license; and the SRO's job performance

was satisfactory

during three watches he stood with this identified

condition, and these factors will be considered

prior to a final severity level determination.

Each of the two events would be considered

violations

of the same regulatory

standard (10 CFR 55.3) and share a common root cause of programmatic

issues within PPL's licensed operator medical reviews. The finding was determined

to have a cross-cutting

aspect in the area of Problem Identification

and Resolution, Operating

Experience, because PPL did not systematically

collect, evaluate, and communicate

relevant external operating

experience

P.2(a).

Specifically, PPL failed to properly evaluate IN 2004-20 for medical examination

issue applicability

in accordance

with their operating

experience

review program as evidenced

by the 2008 SL-IV NCV (NRC IR 50-387 & 50-388 2008302-01), for an initial licensed operator application

submitted

to the NRC with a disqualifying

medical condition, as well as these two events in July and August of 2009. Enclosure

Enforcement:

Event 1: 10 CFR 55.21 requires, in part, that "a licensee shall have a medical examination

by a physician

every two years. The physician

shall determine

that the applicant

or licensee meets the requirements

of 10 CFR 55.33(a)(1).

10 CFR 55.33(a)(1)

states, in part, that the applicants

medical condition

and general health will not adversely

affect the performance

of assigned job duties or cause operational

errors endangering

public health and safety. 10 CFR 55.3 states that, "A person must be authorized

by a license issued by the Commission

to perform the function of an operator or a senior operator as defined in this part". Contrary to the above, between April 1, 2009, and July 22, 2009, PPL failed to ensure that the individual

licensee, an SRO, while on shift, was authorized

by a license to perform the function of an SRO, after he failed to have the required two-year medical examination.

Specifically, the SRO performed

licensed operator duties 52 times between April 1, 2009, and July 22, 2009, after the deadline for his medical examination

had passed. The medical examination

may have identified

an issue with the SRO's medical condition

and general health that would have disqualified

him from being authorized

by a license. Event 2: 10 CFR 55.21 requires, in part, that a licensee shall have a medical examination

by a physician

every two years. The physician

shall determine

that the applicant

or licensee meets the requirements

of 10 CFR 55.33{a)(1).

10 CFR 55.33(a){1)

states, in part, that the applicant's

medical condition

and general health will not adversely

affect the performance

of assigned job duties or cause operational

errors endangering

public health and safety. 10 CFR 55.33(b) states, in part, if an applicant's

general medical condition

does not meet the minimum standards

under 10 CFR 55.33(a)(1)

the Commission

may approve the application

and include conditions

in the license to accommodate

the medical defect. 10 CFR 55.23(b) states in part, when the certification

requests a conditional

license based on medical evidence, the medical evidence must be submitted

to the Commission

and the Commission

then makes a determination

in accordance

with 10 CFR 55.33. 10 CFR 55.3 states that a person must be authorized

by a license issued by the Commission

to perform the function of an operator or a senior operator as defined in this part. Contrary to the above, between August 10,2009, and August 18, 2009, PPL failed to ensure that the individual

licensee, an SRO, while on-shift, was authorized

by a license to perform the function of an SRO, after he failed a medical examination

which identified

a disqualifying

condition.

Specifically, a medical examination

conducted

on August 10, 2009, identified

that the SRO's vision did not meet the health requirements

stated in ANSI/ANS 3.4-1983, Section 5.4.5, "Eyes." However, he performed

the function of an SRO during three watches with a license that was not appropriately

conditioned

to

that corrective

lenses be worn. Each example was evaluated

independently

using the traditional

enforcement

process because the failure to determine

an operator's

medical condition

and general health has the potential

to impact or impede the regulatory

process. Specifically, medical certification

and conditional

licensing

are used by the NRC to ensure health conditions

Enclosure

will not adversely

affect operator duties or performance. (AV 05000387;

02, Violation

of 10CFR55.3, Senior Reactor Operators

Performing

Licensed Duties While Not Qualified

Due to Medical Examination

Issues) Maintenance

Effectiveness

(71111.120 -3 Samples) a. Inspection

Scope Tile inspectors

evaluated

PPL's work practices

and follow-up

corrective

actions for selected structures, systems and components (SSC) issues to assess the effectiveness

of PPL's maintenance

activities.

The inspectors

reviewed the performance

history of those SSCs and assessed PPL's extent of condition

determinations

for these issues with potential

common cause or generic implications

to evaluate the adequacy of PPL's corrective

actions. The inspectors

reviewed PPL's problem identification

and resolution

actions for these issues to evaluate whether PPL had appropriately

monitored.

evaluated.

and dispositioned

the issues in accordance

with PPL procedures

and the requirements

of 10 CFR 50.65, "Requirements

for Monitoring

the Effectiveness

of Maintenance." In addition, the inspectors

reviewed selected SSC classification, performance

criteria and goals, and PPL's corrective

actions that were taken or planned. to verify whether the actions were reasonable

and appropriate.

Documents

reviewed are listed in the Attachment.

The following

issues were reviewed: Unit 1, HPCI turbine stop valve failure and previous corrective

actions for inadequate

preventative

maintenance; Multiple failures of EDG air start system relief valves which caused "A" EDG unavailability;

and Station blackout (SBO) diesel generator (DG) unavailability

due to radiator coolant leakage. b. Findings Introduction:

The inspectors

identified

a Green NCVof 10 CFR Part 50, Appendix B. Criterion

XVI. "Corrective

Action," in that, PPL did not implement

timely corrective

actions to preclude repetition

of a significant

condition

adverse to quality. Specifically, the actions taken to address the causes of the Unit 1 HPCI stop valve failure to close in 2006 did not prevent the same Unit 1 HPCI stop valve from failing to close on August 18, 2009. In both cases, the failure of the stop valve to close rendered this single train high pressure injection

system inoperable

as it was unable to meet the 30 second injection

response time as described

in the design basis. Discussion:

On August 18, 2009, the Unit 1 HPCI stop valve (FV-15612)

indicated

dual position after performance

of the weekly lubricating

oil functional

check. FV-15612 did not go full closed as expected and was verified to be approximately

one inch from full closed. Operations

cycled the valve with maintenance

personnel

present in the field and found that the valve did not operate smoothly when closing. Based on previous history with FV-15612, engineering

recommended

that the HPCI system be declared inoperable.

Unit 1 HPCr was declared inoperable

and the FV15612 valve was disassembled

and repaired.

The failure of FV-15612 Significantly

impacts HCpr operation

because the HPCI ramp generator

resets to idle when the lower limit switch opens (at the full closed indication

on Enclosure

FV-15612).

Thus, FV-15612's

closure is necessary

to prepare the governor to restart the turbine and if FV-15612 does not fully close, the generator

can not reset, and the governor would demand full open when the turbine restarts.

This condition

greatly increases

the probability

of an overspeed

trip upon turbine start. Historical

data from the original HPCI speed control design reveals that it would be expected to have at least 1 or 2 overspeed

trips before the HPCI governor would be able to control turbine speed. In this condition

the HPCI 30 second design basis response time would not be met. (Ref: TS 3.5.1.13).

Therefore, HPCI was not able to perform its safety function with design limits and was inoperable.

In addition, this degraded component

also challenges

the system protective

features {overspeed

trip function}

which reduces the reliability

of the system to function.

The safety system remained unavailable

for several days as extensive

effort was required to repair the component

for this type of degradation.

Inspectors

witnessed

some of the maintenance

work and observed that there were many physical similarities

to the conditions

found when this valve was disassembled

and repaired following

the failure to close in August of 2006. One documented

cause for the 2006 FV-15612 failure was an observed seal area that is periodically

wetted by HPCI operation

and a material which is susceptible

to general corrosion

and requires periodic replacement

to maintain proper operation.

In 2006, PPL took the action to replace the rod bushing. However, there were no actions to address the cause and reduce moisture exposure, change or evaluate materials

to reduce the susceptibility

to corrosion, and no actions to increase component

monitoring

for moisture or corrosion.

The second documented

apparent cause for the 2006 FV-15612 failure was inadequate

preventive

maintenance (PM). An administrative

error had caused this component

to go past the PM expiration

date. PPL performed

the inspections

as part of the 2006 repair and recalculated

a new due date for the PM task. PPL did not change the 10 year interval for maintenance

and inspection

and did not increase the PM frequency

for this component

to more appropriately

address this identified

apparent cause (inadequate

PM). The inspectors

determined

that the limited corrective

actions taken following

the apparent cause evaluation

in 2006 contained

in CR 806988 were a primary contributor

to the repeat failure of the FV-15612 in 2009. In both cases, valve FV15612 failed in the same manner and would not travel to the full closed position.

In both cases, the actuator stem to bushing interface

was very tight and required the use of pullers and/or hammers during actuator disassembly.

For both failures the most likely cause was due to increased

friction between the actuator shaft and the rod bushing as a result of corrosion.

The inspectors

also identified

that the corrective

action report CR 806988 did not have an effectiveness

review plan. The CR stated that given the long duration of the PM interval, it would be unreasonable

to hold an effectiveness

review open for several years. The inspectors

reviewed PPL's cause evaluation

for the August 2009 valve failure, as documented

in CR 1172997. This evaluation

described

how the leakage through the seat of the Unit 1 HPCI Steam Admission

Valve (HV-155F001)

was a contributing

cause to the 2009 component

failure. The HV-155F001

had chronic through seat leakage for the last decade. Inspectors

concluded

that this leakage and moisture source was also a contributing

factor from 2006, and that more aggressive

action to fix the seat leakage which contributed

to the corrosive

environment

would have reduced the probability

and/or frequency

of the experienced

component

failure. Enclosure

Analysis:

The finding is more than minor because it adversely

affected the equipment

pE:lrformance

attribute

of the Mitigating

Systems cornerstone

objective, to ensure the availability, reliability

and capability

of equipment

that respond to initiating

events to prevent undesirable

consequences.

Specifically, with FV-15612 unable to fully close, the HPCI 30 second design basis response time would not be met. Not only did this dE3graded

component

make the HPCI system inoperable;

it also challenged

the system protective

features (overspeed

trip function)

which reduced the reliability

of the system to function.

In addition, the repairs necessary

to restore the system required extensive

effort and resulted in several days of unplanned

unavailability

for a single train safety system. The inspectors

assessed this finding in accordance

with IMC 0609 Attachment

4, "Phase 1 -Initial Screening

and Characterization

of Findings" and determined

the finding to be of very low safety significance (Green) because it did not result in an actual loss of safety function for greater than the TS allowed outage time. The finding was not potentially

risk Significant

due to seismic, flood, or severe weather initiating

events. This finding was determined

to have a cross-cutting

aspect in the area of Problem Identification

and Resolution, Corrective

Action Program, because PPL did not take appropriate

corrective

actions to address safety issues in a timely manner, commensurate

with their safety Significance

and complexity

[P.1 (d)]. Specifically, PPL did not take appropriate

corrective

actions for a significant

condition

adverse to quality from the 2006 failure of the HPCI stop valve to prevent the 2009 failure of the same valve. Enforcement:

10 CFR Part 50, Appendix B, Criterion

XVI, "Corrective

Action," requires, in-part, for significant

conditions

adverse to quality, measures shall assure that the cause of the condition

is determined

and corrective

action taken to preclude repetition.

Contrary to the above, PPL did appropriately

identify several causes but corrective

actions following

the 2006 valve failure did not prevent repetition

of the same HPCI stop valve failure on August 18, 2009. In both cases, the failure of the stop valve to close rendered this single train high pressure injection

system inoperable

as it was unable to meet the 30 second injection

response time as described

in the design basis. In 2009 this particular

failure also caused several days of unplanned

unavailability

due to the extensive

effort to repair the component.

Because the finding is of very low safety significance

and has been entered into PPL's CAP (CR 710737), this violation

is being treated as a Non-Cited

Violation (NCV), consistent

with Section VI.A of the NRC Enforcement

Policy. (NCV 05000387/2009004-03, Inadequate

Corrective

Actions Result in a Repeat Failure of Unit 1 HPCI Turbine Stop Valve). 1 R 13 Maintenance

Risk Assessments

and Emergent Work Control (71111.13 7 Samples) a. Inspection

Scope The inspectors

reviewed the assessment

and management

of selected maintenance

activities

to evaluate the effectiveness

of PPL's risk management

for planned and emergent work. The inspectors compared

the risk assessments

and risk management

actions to the requirements

of 10 CFR Part 50.65(a)(4)

and the recommendations

of NUMARC 93-01, Section 11, "Assessment

of Risk Resulting

from Performance

of Maintenance

Activities." The inspectors

evaluated

the selected activities

to determine

Enclosure

whether risk assessments

were performed

when specified

and appropriate

risk management

actions were identified.

The inspectors

reviewed scheduled

and emergent work activities

with licensed operators

and work-coordination

personnel

to evaluate whether risk management

action threshold

levels were correctly

identified.

In addition, the inspectors

compared the assessed risk configuration

to the actual plant conditions

and any in-progress

evolutions

or external events to evaluate whether the assessment

was accurate, complete, and appropriate

for the emergent work activities.

The inspectors

performed

control room and field walkdowns

to evaluate whether the compensatory

measures identified

by the risk assessments

were appropriately

performed.

Documents

reviewed are listed in the Attachment.

The selected maintenance

activities

included: Unit 1, 2-4 GPM leak on RWCU filter demineralizer

outlet isolation

valve emergent work control; Unit 1, Yellow Risk during corrective

maintenance

on SBO DG concurrent

with Unit 1 HPCI stop valve and "B" EDG jacket water heater failures on August 21; Units 1 and 2, 2A residual heat removal service water (RHRSW)

pump inoperable

due to loose electrical

junction box supports concurrent

with Unit 1 RHRSW subsystem

inoperable

for scheduled

maintenance;

dual unit 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> shutdown limiting condition

for operation (LCO); Orange equipment

out-of-service

risk for both Unit 1 and Unit 2 during "A" EDG outage and emergent "E" EDG inoperability, CR 1165553; Replace recirculation/standby

gas treatment

system (SGTS) damper actuator;

dual unit 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> shutdown LCO; Emergent wiring repairs on ESS transformer

OX203 in 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> LCO; and T20 startup transformer (T20) high voltage bushing replacement

and Bus 20 clean and inspect. b. Findings No findings of significance

were identified.

1 Operability

Evaluations

(71111.15 -7 Samples) a. Inspection

Scope The inspectors

reviewed operability

determinations

that were selected based on risk insights, to assess the adequacy of the evaluations, the use and control of compensatory

measures, and compliance

with TSs. In addition, the inspectors

reviewed the selected operability

determinations

to evaluate whether the determinations

were performed

in accordance

with NDAP-QA-0703, "Operability

Assessments." The inspectors

used the TSs, Technical

Requirements

Manual, Final Safety Analysis Report (FSAR), and associated

DeSign Basis Documents

as references

during these reviews. Documents

reviewed are listed in the Attachment.

The issues reviewed included: Unit 1, RHR Oivision I, gas entrainment

issue; Unit 1, repeat failure of 1 B RHRSW pump 1ST; Unit 2, '0' main steam line radiation

monitor on multiple alarms and work orders; Enclosure

.1 Unit 2, HPCI operators

disabled auxiliary

oil pump during surveillance

restoration

steps on May 16, 2009; Common cause analysis after "C" EDG trip on overspeed; <IE" EDG with failed turbocharger

overspeed

speed trip circuit, OFR 1166085; and "0" EDG, ESW piping clamp support on floor, CR 1181216. b. Findings No findings of significance

were identified

1 Plant Modifications

(71111.18 -2 Samples) T,emporary

Plant Modifications

(1 Sample) a. Inspection

Scope The inspectors

reviewed a temporary

plant modification

to determine

whether the change adversely

affected system or support system availability, or adversely

affected a function important

to plant safety. The inspectors

reviewed the associated

system design bases, including

the FSAR, TSs, and assessed the adequacy of the safety determination

screening

and evaluation.

The inspectors

also assessed configuration

control of the change by reviewing

selected drawings and procedures

to verify whether appropriate

updates had been made. The inspectors

compared the actual installation

to the temporary

modification

documents

to determine

whether the implemented

change was consistent

with the approved documents.

The inspectors

reviewed selected post-installation

test results to determine

whether the actual impact of the change had been adequately

demonstrated

by the test. Documents

reviewed are listed in the Attachment.

The following

modification

and document was included in the review: Unit 1, Temporary

Engineering

Change 1136133, bypass gas discharge

temperature

trip on 1 K206B. b. Fr:ndings

No findings of significance

were identified . . Permanent Plant Modifications

(1 Sample) a. Inspection

Scope The inspectors

reviewed a permanent

plant modification

to determine

whether the change adversely

affected system or support system availability, or adversely

affected a function important

to plant safety. The inspectors

reviewed the associated

system design bases, including

the FSAR, TSs, and assessed the adequacy of the safety determination

screening

and evaluation.

The inspectors

also assessed configuration

control of the change by reviewing

selected drawings and procedures

to verify whether appropriate

updates had been made. The inspectors

compared the actual installation

to the permanent

modification

documents

to determine

whether the implemented

change was consistent

with the approved documents.

The inspectors

reviewed selected Enclosure

post-installation

test results to verify whether the actual impact of the change had been adequately

demonstrated

by the test. Documents

reviewed are listed in the Attachment.

The following

modification

and document was included in the review: Engineering

Work Request 1086364, T20 H1 bushing replacement.

b. Findings No findings of significance

were identified. Post-Maintenance

Testing (71111.19-

6 Samples) a. Inspection

Scope The inspectors

observed portions of post-maintenance

test (PMT) activities

in the field to determine

whether the tests were performed

in accordance

with the approved procedures.

The inspectors

assessed the test adequacy by comparing

the test methodology

to the scope of maintenance

work performed.

In addition, the inspectors

evaluated

acceptance

criteria to determine

whether the test demonstrated

that components

satisfied

the applicable

design and licensing

bases and TS requirements.

The inspectors

reviewed the recorded test data to determine

whether the acceptance

criteria were satisfied.

Documents

reviewed are listed in the Attachment.

The PMT activities

reviewed included: Unit 1, HPCI PMT after stop valve repair; Unit 1, single control rod scram during scram switch functional

check; Unit 1, core spray valve exercising, HV152F0005A

and F015A after breaker swaps; Unit 2, reactor core isolation

cooling (RCIC) pump and flow testing and overspeed

trip test following

resolution

of turbine trip tappet nut alignment, CR 1146099; Unit 2, PMT of PSV 251 F087 after maintenance

to eliminate

emergency

core cooling system keepfill leakage past valve; and T20 high bushing replacement, tap charger inspection

and bus 20 cleaning and inspection.

b. Findings No findings of significance

were identified. 1 Surveillance

Testing (71111.22

-4 Routine Surveillance

and 1 1ST Samples) a. Inspection

Scope The inspectors

observed portions of selected surveillance

test activities

in the control room and in the field and reviewed test data results. The inspectors

compared the test results to the established

acceptance

criteria and the applicable

TS or Technical

Requirements

Manual operability

and surveillance

requirements

to evaluate whether the systems were capable of performing

their intended safety functions.

Documents

Enclosure

21 reviewed are listed in the Attachment.

The observed or reviewed surveillance

tests included: Unit 1, quarterly

functional

test of reactor vessel water level channels LlS-B21-IN031A, 3B, C, D, SI-180-203; Unit 2, 1ST testing of RCIC pump flow indication

from remote shutdown panel; "A" SGTS filter and absorber leak tests; "D" EDG full load rejection

test, SE-024-D01;

and Monthly operation

of SGTS train "A", SO-070-001.

b. Findings No findings of significance

were identified.

1 Drill Evaluation

(71114.06 -1 Sample) a. Inspection

Scope Tlhe inspectors

reviewed the combined functional

drill scenario (2009 Gold Team Emergency

Drill) that was conducted

on August 25, 2009, and observed selected portions of the drill in the simulator

control room and technical

support center. The inspection

focused on PPL's ability to properly conduct emergency

action level classification, notification, and protective

action recommendation

activities

and on the evaluators'

ability to identify observed weaknesses

and/or deficiencies

within these areas. Ten performance

indicator (PI) opportunities

were included in the scenario.

The inspectors

attended the evaluators'

post-drill

critique and compared identified

weaknesses

and deficiencies

including

missed PI opportunities

against those identified

by PPL to determine

whether PPL was properly identifying

weaknesses

and failures in tbese areas. Documents

reviewed are listed in the Attachment.

b. Findings No findings of significance

were identified. RADIATION

SAFETY Cornerstone:

Occupational

Radiation

Safety (OS) Access Control to Radiologically

Significant

Areas (71121.01

6 Samples) a. Inspection

Scope The inspectors

reviewed and assessed the adequacy of PPL's internal dose assessment

for any actual internal exposure greater than 50 mrem committed

effective

dose equivalent.

The inspectors

examined PPL's physical and programmatic

controls for highly activated

or contaminated

materials (non-fuel)

stored within spent fuel and other storage pools. Enclosure

For high radiation

work areas with significant

dose rate gradients (factor of 5 or more), the inspectors

reviewed the application

of dosimetry

to effectively

monitor exposure to pE!rSOnnel.

The inspectors

discussed

with the radiation

protection

manager high dose rate-high

radiation

area, and very high radiation

area controls and procedures.

The inspectors

focused on any procedural

changes since the last inspection.

The inspectors

verified that any changes to PPL's procedures

did not substantially

reduce the effectiveness

and level of worker protection.

The inspectors

discussed

with health physics supervisors

the controls in place for special areas that have the potential

to become very high radiation

areas during certain plant operations.

The inspectors

determined

that these plant operations

required communication

beforehand

with the health physics group, so as to allow corresponding

timely actions to properly post and control the radiation

hazards. The inspectors

verified adequate posting and locking of entrances

to high dose rate-high

radiation

areas, and very high radiation

areas. The inspectors

evaluated

PPL's performance

against the requirements

contained

in 10 CFR 20 and Plant Technical

Specification

5.7. Documents

reviewed are listed in the Attachment.

b. Findings No findings of significance

were identified.

20S2 ALARA Planning and Controls (71121.02

-3 Samples) a. Inspection

Scope The inspectors

obtained from PPL a list of work activities

ranked by actual/estimated

exposure that are in progress or that have been completed

during the last outage and select the 2 work activities

of highest exposure

significance (in-vesseIISIIIVVI

and EPU alternate

decay heat removal modification).

The inspectors

reviewed PPL's method for adjusting

exposure estimates, or re-planning

work, when unexpected

changes in scope or emergent work are encountered.

The inspectors

evaluated

whether adjustments

to estimated

exposure (intended

dose) were based on sound radiation

protection

and ALARA principles

or just adjusted to account for failures to control the work. The inspectors

evaluated

PPL's performance

against the requirements

contained

in 10 CFR 20.1101. Documents

reviewed are listed in the Attachment.

Enclosure

b. Findings Introduction:

A self-revealing

Green finding was identified

due to a deficiency

in the area of maintaining

occupational

radiation

exposures

ALARA. Work performance

involving

the IWI/ISI during the Unit 2 14th Refuel and Inspection

Outage was less than adequate resulting

in collective

exposure for the work to expand from 5.00 person-rem

to 11.04 person-rem.

Description:

The IWI/ISI dose overrun was primarily

due to the utilization

of inexperienced

contract workers to perform the task. The contractor

selected by PPL utilized workers for major IWIIISI tasks, including:

inspection;

camera placement

and repair; and, pressure washing/surface

preparation, were inexperienced

in performing

these tasks. The work hours to perform these tasks then expanded to include an additional

294 hours0.0034 days <br />0.0817 hours <br />4.861111e-4 weeks <br />1.11867e-4 months <br /> for inspection;

207 hours0.0024 days <br />0.0575 hours <br />3.422619e-4 weeks <br />7.87635e-5 months <br /> for camera placement

and repair; and, 1000 hours0.0116 days <br />0.278 hours <br />0.00165 weeks <br />3.805e-4 months <br /> for pressure washing/surface

preparation.

These examples of additional

high radiation

work resulted in additional

collective

exposure that could have been avoided had sufficient

pre-job training been provided.

Pre-task training for workers, as described

in the pre-outage

work plan, was inadequate

for the tasks to be performed, based on the use of inexperienced

workers. Outage planning for this work was based upon past performance

in earlier outages with experienced

work crews, and estimated

to require less than 3000 hours0.0347 days <br />0.833 hours <br />0.00496 weeks <br />0.00114 months <br />. Actual hours to perform these tasks with the inexperienced

workers were over 5000 hours0.0579 days <br />1.389 hours <br />0.00827 weeks <br />0.0019 months <br />. The original exposure estimate was 5.00 person-rem.

When compared to the actual work activity exposure of 11.04 person-rem, the results were 120 percent greater

than the exposure estimate.

Analysis:

Inadequate

work planning that resulted in significant

unplanned

collective

exposure was a performance

deficiency

which was reasonably

within PPL's ability to foresee and correct and which should have been prevented.

Specifically, the original exposure estimate was 5.00 person-rem.

When compared to the actual work activity exposure of 11.04 person-rem, the results were 120 percent greater than the exposure estimate.

The finding is more than minor because the issue involved actual collective

exposure greater than 5 person-rem

that was greater than 50 percent above the estimated

or intended exposure and the dose overrun was due to activities

within PPL's control. This issue is similar to the greater than minor examples provided in Appendix E of Manual Chapter 0612. Further, the performance

deficiency

is associated

with the radiation

safety cornerstone

attribute

of the program (ALARA planning)

and adversely

affected the cornerstone

objective

to ensure adequate protection

of worker health and safety from exposure to radiation.

The finding was evaluated

in accordance

with IMC 0609, Appendix C, "Occupational

Radiation

Safety Significance

Determination

Process." The inspectors

determined

that the finding was of very low safety significance (Green) because: (1) it involved an ALARA planning issue, and (2) the 3-year rolling average collective

dose history was less than 240 person-rem

(107 person-rem

annual exposure for 2005-2007).

This finding was entered into PPL's CAP (CR 1140623 and 1137835).

This finding was determined

to have a cross-cutting

aspect in the area of Human Performance, Resources, because PPL did not utilize sufficiently

qualified

personnel

to assure occupational

radiation

safety requirements

were met H.2(b).

Specifically, PPL's use of inexperienced

contract workers resulted in additional

collective

exposure that could have been avoided. Enclosure

Enforcement:

Enforcement

action does not apply because the performance

deficiency

did not involve a violation

of regulatory

requirement.

The ALARA rule contained

in 1 (I CFR 20.1101 (b) Statements

of Consideration

indicates

that compliance

with the ALARA requirement

will be judged on whether the licensee has incorporated

measures to track and, if necessary, to reduce exposures

and not whether exposures

and doses represent

an absolute minimum or whether the licensee has used all possible methods to reduce exposures.

The overall exposure performance

of the nuclear power plant is used to determine

compliance

with the ALARA rule. Since SSES is below the year-rolling-average

of 240 person-rem

and PPL has an established

ALARA program to reduce exposure consistent

with the statements

of consideration

for 10 CFR 20.1101, no violation

of regulatory

requirements

[10 CFR 20.11 01 (b)] is considered.

Because this finding does not involve a violation

of regulatory

requirements

and has very low safety significance, it is identified

as (FIN 05000388/2009004-04, Failure to Maintain Occupational

Radiation

Exposure as Low as Reasonably

Achievable

during the Unit 2 Refueling

Outage) 20S3 Radiation

Monitoring

Instrumentation

(71121.03

-1 Sample) a. Inspection

Scope The inspectors

verified the calibration, operability, and alarm setpoints

of several types of instruments

and equipment.

Verification

methods included:

review of calibration

documentation

and observation

of PPL's source check or calibrator

exposed readings.

The inspectors

reviewed the detector measurement

geometry, calibration

method and appropriate

selection

of calibration

sources to closely represent

the actual measurement

conditions

in the plant. The inspectors

observed electronic

and radiation

calibration

of these. The inspectors

reviewed the alarm set point determinations

and observed in-field source checks. The inspectors

determined

what actions were taken when, during calibration

or source checks, an instrument

was found significantly

out of calibration

(>50 percent).

The inspectors

determined

the possible consequences

of instrument

use since last successful

calibration

or source check. The inspectors

determined

if the out of calibration

result was entered into the CAP. During an on-site visit, the inspectors

reviewed calibration

data, quality assurance (QA) data and National Voluntary

Laboratory

Accreditation

Program audits and intercomparison

test data for PPL's personnel

dosimetry

laboratory

located in Allentown.

The inspectors

evaluated

PPL's performance

against the requirements

contained

in 10 CFR 20.1501,10

CFR 20.1703 and 10 CFR 20.1704. Documents

reviewed are listed in the Attachment.

b. Findings No findings of significance

were identified.

Enclosure

.1 OTHER ACTIVITIES Performance

Indicator

Verification

(71151 -8 Samples) Injtiating

Events Inspection

Scope The inspectors

reviewed PPL's PI data for the period of August 2008 through August 2009 to verify whether the PI data was accurate and complete.

The inspectors

examined selected samples of PI data, PI data summary reports, and plant records. The inspectors

compared the PI data against the guidance contained

in Nuclear Energy Institute

99-02, "Regulatory

Assessment

Performance

Indicator

Guideline." Documents

reviewed are listed in the Attachment.

The following

PIs were included in this review: Units 1 and 2 unplanned

scrams per 7000 critical hours (IE01); Units 1 and 2 unplanned

power changes per 7000 critical hours (IE03); Units 1 and 2 unplanned

scrams with complications (IE04); Common Occupational

Exposure Control Effectiveness (OR01); and Common RETS/ODCM

Radiological

Effluents (PR01)

No findings of significance

were Identification

and Resolution

of Problems (71152 -1 Sample) Review of Items Entered into the Corrective

Action Program Inspection

Scope As specified

by Inspection

Procedure

71152, Problem Identification

and Resolution, and in order to help identify repetitive

equipment

failures or specific human performance

issues for follow-up, the inspectors performed

screening

of all items entered into PPL's CAP. This was accomplished

by reviewing

the description

of each new action requesUcondition

report and attending

daily management

meetings.

No findings of significance

were identified . Annual Sample: Review of PPL's Progress in Implementing

Corrective

Actions to Address General Work Environment

and Potential

Chilling Effect Concerns Inspection

Scope The inspectors

performed

a detailed review of PPL's corrective

actions associated

with the Root Cause Analysis (RCA) conducted

in response to the NRC's Potential

Chilling Effect (PCE) letter of January 28, 2009 and the associated

action plan. The inspectors

reviewed the RCA, the general work environment

action plan, Employees

Concern Enclosure

26 Program (ECP), QA documents, and selected reference

RCA documents.

The inspectors

also reviewed the corrective

action schedules

and reviewed completed

corrective

actions such as revised procedures, training material, and records. The inspectors

also conducted

interviews

with site ECP and QA personnel, and several focus groups consisting

of workers and supervisors

from the Security, Work Management, Health Physics, and Operations

Departments.

These interviews

were performed

in order to assess how the staff viewed the effectiveness

of the corrective

actions to date in addressing

the general work environment.

The inspectors

also assessed PPL's longer term action plan items by verifying

action item entries in the CAP as well as through interviews

of responsible

personnel.

b. Findings and Observations

No findings of significance

were identified.

Background:

On January 28, 2009, the NRC issued a PCE letter advising PPL of concerns related to the safety conscious

work environment (SCWE) at SSES and requested

PPL provide: (1) a description

of PPL's current action plans to address existing SCWE concerns to preclude a chilled work environment

at SSES; (2) PPL plans for further evaluating

the health of the SCWE at SSES; and (3) the metrics PPL intended to monitor to determine

the effectiveness

of their actions and ensure a SCWE at SSES (ML090280115).

Also, on January 28, 2009, the NRC issued SSES -NRC Integrated

Inspection

Report 05000387/2008005

and 05000388/2008005 (ML090230434)

which described

the SCWE concerns at PPL and provided additional

background.

PPL completed

their formal RCA of the work environment

issues in May 2009. The NRC's review of that RCA is documented

in NRC Integrated

Inspection

Report 05000387/2009003

and 05000388/2009003 (ML092230158).

Root Cause Analysis Corrective

Actions The inspectors

determined

that the corrective

actions developed

by the RCA team to address the root cause and causal factors were being appropriately

scheduled

and that the actions were being completed

in accordance

with that schedule.

The time frame for completion

of these scheduled

actions was also determined

to be appropriate.

Any changes to the schedule required a review by the Management

Review Committee

and approval by senior management.

Corrective

actions completed

to date included the roll out of the RCA through formal site presentations

and small group discussions, the establishment

of two methods

for workers to raise an anonymous

concern (Safety Hotline and anonymous generated

CRs), developing

training materials

and case studies related to work environment

issues and conducting

this training with all first line supervisors

and positions

above, and revising several procedures.

The training was well received by plant personnel

and the new anonymous

concern processes

was being utilized by plant personnel.

In addition, several organizational

changes were made including

the arrival of the new eNO in July 2009, the establishment

of a plant manager position, restructuring

to have QA, ECP, and Regulatory

Affairs directly reporting

to the CNO, and the selection

of several new personnel

for key management

positions.

The inspectors

observed that these changes were well communicated

to the site and generally

have been well Enclosure

received.

Most personnel

interviewed

felt the organizational

changes were appropriate

and the personnel

selected were a good fit for their new positions.

These changes have allowed progress to be made in re-establishing

trust between the workers and upper management

and improving

the general work environment.

Employee Concerns Program Another corrective

action from the RCA was to evaluate and make changes to the ECP. A strong ECP is a pillar of a successful

safety culture. However, in the past at SSES, the ECP was not seen by many plant employees

as a viable and effective

program. During the third quarter 2009, PPL restructured

the ECP program by eliminating

the Ombudsman

position and hiring an additional

ECP representative

who was full time on-site at SSES. The inspectors

interviewed

ECP representatives

and discussed

the ECP program re-organizations

with each of the focus groups. The inspectors

concluded

that PPL did a good job communicating

the changes in the ECP program to the site. All groups interviewed

knew who the new ECP representative

was and were aware that the Ombudsman

position had been eliminated.

Most had a positive impression

and an inherent level of trust for the new on-site ECP representative

selected.

In addition, corrective

actions were completed

changing the organizational

reporting

requirements, taking the ECP program out to the line organization

and making it a direct report to the CNO. However, additional

organizational

changes in the ECP Oversight

Team remain to ensure that the ECP process is viewed by the workforce

as a viable alternative

for issues. See NRC Integrated

Inspection

Report 05000387/2009003

and 05000388/2009003 (ML092230158)

for further details on this concern. Challenges:

The inspectors

identified

two upcoming challenges

which have the potential

to impact the general work environment.

The first challenge

will be the implementation

of the NRC Fatigue Rule (10 CFR 26 Subpart I) which went into effect October 1,2009. The inspectors

observed that the plant had done a good job communicating

the new rule, and had done a good job working with the departments

most heavily impacted (Operations

and Security);

however, several workers and supervisors

interviewed

expressed

uncertainty

as to how the rule will be implemented

and what will be the true impact. PPL acknowledged

it was slow in engaging the bargaining

unit regarding

potential

shift rotation adjustments

in the Health Physics Department, which was a concern to the mc:ijority

of the Health Physics personnel

interviewed.

In a similar note, the upcoming collective

bargaining

unit negotiations

have the potential

to impact the general work environment.

Assessment

During the 3 rd quarter of 2009, PPL made reasonable

process in implementing

their action plan and RCA corrective

actions to address the general work environment

at SSES. Based on interviews

with a sample population

of site employees, the actions to date have been well received and are making a positive impact on the general work environment

at SSES. Overall, the workers stated they were cautiously

optimistic

that changes were being implemented;

however, they acknowledged

that significant

work remained to be done and several Significant

challenges

still need to be addressed.

The NRC plans to continue monitoring

PPL's progress in this area. Enclosure

.1 40A5 Other Activities

Quarterly

Resident Inspector

Observations

of Security Personnel

and Activities

a. Inspection

Scope During the inspection

period, the inspectors

conducted

observations

of security force personnel

and activities

to ensure that the activities

were consistent

with licensee security procedures

and regulatory

requirements

relating to nuclear plant security.

These observations

took place during both normal and off-normal

plant working hours. b. Findings No findings of Significance

were identified . . 2 Independent

Spent Fuel Storage Installation

(60855 and 60855.1) a. Inspection

Scope The inspectors

observed selected activities

associated

with loading of a dry cask canister to ensure that TSs were met and equipment

operated properly.

The inspectors

reviewed documents

and records associated

with the operation

of the SSES independent

spent fuel storage installation (ISFSI), including

training records for personnel

involved with loading of a dry cask canister.

A list of the documents

reviewed is provided in the Supplemental

Information

section. The inspectors

met with reactor engineering

personnel

to review the fuel selection

process and associated

documentation.

The inspectors

discussed

how the cask loading computer program is created for each cask loading. The video recording

of the fuel bundles placed into the canister was reviewed to ensure that each bundle was placed into the proper location.

The inspectors

observed work activities

on the refuel floor associated

with the fuel selection, loading of fuel into the cask, vacuum drying, welding, and moving of the loaded canister to the truck bay. b. Findings No findings of significance

were identified.

However, the inspectors

did identify an issue regarding

compliance

with procedure

MT-GM-014, "Rigging and Lifting Equipment

Inspection." This procedure

references

ASME code 830.9-2003, "Slings." Both documents

require that slings are to be inspected

annually.

While the licensee also performs an inspection

of each sling prior to use in accordance

with the same procedure, the pre-job inspection

does not meet the annual inspection

requirement.

Inspectors

noted that when synthetic

slings used in dry cask storage are inspected

by PPL they receive an August 5 th due date sticker for the following

year, regardless

of when they are inspected

in the current year. This presented

a potential

for a sling to exceed its annual inspection

based on the annotated

date. PPL entered this issue into their corrective

action program under CR 1173698, "SSES Rigging Committee

review of procedural

guidance." The licensee's

extent of condition

review did not identify any slings used in safety related activities

which had actually exceeded the annual inspection

criteria.

As a result, this issue was determined

to be of minor significance

and a violation

of minor significance

that is not subject to enforcement

action in accordance

with the NRC's Enforcement

Policy. However, for assessment

purposes, this issue does Enclosure

.3 illustrate

a weakness in PPL's Corrective

Action Program because it did not identify a non compliance

with a regulatory

requirement.

Operation

of an ISFSI at Operating

Plants (60855) a. Inspection

Scope The inspectors

verified by direct observation

and independent

evaluation

that PPL had performed

loading activities

at the ISFSI in a safe manner and in compliance

with applicable

procedures.

This included observing

the loading of one canister of spent fuel into the ISFSI on August 10, 2009. The inspectors

verified by direct observation

that radiation

dose and contamination

levels were within prescribed

limits after a dry cask storage system container

had been installed

at the ISFSI. b. Findings No findings of significance

were identified.

40A6 Meetings, Including

Exit On August 14, 2009, the health physics inspector

presented

inspection

results to Mr. C. Gannon and other members of his staff, who acknowledged

the findings.

The inspector

confirmed

that proprietary

information

was not provided or examined during the inspection.

On August 21,2009, the health physics inspectors

presented

inspection

results to Mr. C. Gannon and other members of his staff, who acknowledged

the findings.

The inspectors

confirmed

that proprietary

information

was not provided or examined during the inspection.

On October 9,2009, the resident inspectors

presented

their findings to Mr. T. Rausch, and other members of his staff, who acknowledged

the findings.

The inspectors

confirmed

that proprietary

information

was not provided or examined during the inspection.

40A7 Licensee-Identified

Violations

The following

violation

of very low safety significance (Green) was identified

by PPL and is a violation

of NRC requirements

which meets the criteria of Section VI of the NRC Enforcement

Policy, NUREG-1600, for being dispositioned

as an NCV: On 25 August 2009, while performing

pre-start

checks to place Unit 2 RHR in suppression

pool cooling, a field operator identified

the ESW cooling water valves 211193 and 211194 to be unlocked and closed. These valves are required to be locked open to assure supply of cooling to a Unit 2 RHR room cooler and 2C RHR pump motor oil cooler. This was an identified

violation

of TS 5.4.1, and a violation

of those procedures

that must be implemented

for operation

of the unit and for the performance

of maintenance

as delineated

in Regulatory

Guide 1.33. Contrary to NDAP-QA-0302, "System Status and Enclosure

Equipment

Control," PPL did not use a proceduralized

method to maintain status control of these valves and contrary to NDAP-QA-502, "Work Control Process," these valves were not returned to the original design configuration

following

maintenance.

PPL determined

that the status control of these valves was most likely lost during the post-modification

testing performed

in late April 2009. Upon discovery, the valves were promptly aligned to provide cooling flow and the performance

issue was captured in CR 1174837. Using a Phase III risk evaluation

model, the region staff determined

this finding to be of very low safety significance (Green). A IT ACHMENT: SUPPLEMENTAL

INFORMATION

Enclosure

SUPPLEMENTAL

INFORMATION

KEY POINTS OF CONTACT Licensee Personnel

N. D'Angelo, Manager, Station Engineering

R. Doty, Radiation

Protection

Manager T Iliadis, GM -Nuclear Operations

S. Ingram, Dosimetry

Supervisor

R. Kessler, Health Physicist -

ALARA A. Klopp, Heat Exchanger

Program Engineer D. Leimbach, Eddy Current Level III, In-service

Inspection

R. Pagodin, GM -Nuclear Engineering

G. Ruppert, GM -Work Management

S. Davis, Fire Protection

Program Engineer LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened 05000387;

388/200900402 Violation

of 10CFR55.3, Senior Reactor Operators

Performing

Licensed Duties While Not Qualified

Due to Medical Examination

Issues (1 R11.2) Opened/Closed

05000388/200900401 Failure to Implement

and Maintain the Fire Protection

Program with Respect to the Use and Storage of Combustibles

in the Control Structure

(1 R05) 05000387/200900403 Inadequate

Corrective

Actions Result in a Repeat Failure of Unit 1 HPCI Turbine Stop Valve (1R12) 05000388/200900404 Failure to Maintain Occupational

Radiation

Exposure As Low As Reasonably

Achievable

during the Unit 2 Refueling

Outage (20S2) Attachment

A-2 BASELINE INSPECTION

PROCEDURE

PERFORMED

LIST OF DOCUMENTS

REVIEWED (Not Referenced

in the Report) Section 1 R04: Equipment

Alignment

Condition

1168300, 1175048, 1176331,

OP-225-001, Containment Instrument

Gas System. Revision CL-225-0012, Unit 2 Containment

Instrument

Gas Mechanical, Revision

M-2126, Unit 2 Containment

Instrument

Gas Sheets 1 and 2, Revision 33 and M-157, Unit 1 Containment

Atmosphere

Control, Revision 47 M-134, A-D Diesel Auxiliaries

Fuel Oil, Lube Oil. Air Intake and Exhaust and Jacket Water Cooling System. Revision 45 Engineering

Work Request: EWR 1168578 Other: Chemistry

Analysis and Sample Results Attached to CR 1167146 Drainage Contour Map, Potentiometric

Surface Contours Overburden

Monitoring

Wells August/September

2008 Section 1 R05: Fire Protection

Condition

Reports: 1172702 Procedures:

FP-113-113, Containment

Access Area (1-401, 1-404, 1-405) Fire Zones 1-4A-N, S, W, Elevation

719'-0", Revision 6 FP-013-168, Equipment

and Battery Rooms Unit 1 West Side (C-605, 606, 600,601,607)

Fire Zones 0-28B-11, 0-28K, 0-28L, 0-281, Elevation

771'-0", Revision 5 FP-013-169, Equipment

and Battery Rooms Unit 1 East Side (C-604, 602, 603, 608) Fire Zones 0-28B1, 0-28M, 0-28N, 0-28J, Elevation

771'-0", Revision 4 Attachment

A-3 Section 1 R06: Flood Protection

Measures Condition

Reports: 1121942,1171337,1172365,and606589

Work Order: 606837 Section 1 R07: Heat Exchanger

Performance

Condition

Reports and Action Requests:

1003096,915409,984635,1136415,1153052, 1178867, 1095358, 1109759, 1172704,892305, 1095358,1109759,1162322,1084289, 1162414, 1108376, and 1044430 Procedures:

H-1001, Heat exchanger

tube cleaning, Revision 5 H-1004, Heat exchanger

inspection

and condition

assessment, Revision 6 H-1005, Eddy Current Examination

Services, Revision 6 NDAP-QA-0504, Heat Exchanger

Program, Revision 4 TP-149-079, RHR Heat Exchanger

Performance

Test, Revision1

ER-AA-340, GL 89-13 Program Implementing

Procedure, Revision 4 ER-AA-340-1001, GL 89-13 Program Implementation

Instructional

Guide, Revision 6 ER-AA-5400, Buried Pipe and Raw Water Corrosion

Program Guide, Revision 1 ER-AA-5400-1001, Raw Water Corrosion

Program Guide, Revision 0 ER-AA-5400-1002, Buried Piping Examination

Guide, Revision 1 Limerick GL 89-13 Program

Basis Document, Revision 0 CY-LG-120-828, Clam Control Activities, Revision 5 CY-LG-120-1102, Outside Chemistry/NPDES

related Sampling and analysis schedule, R:evision

18 CY-LG-120-1117, Spray Pond Chemistry

Guide, Revision 2 ST-2-011-390-0, ESW/Diesel

Generator Heat Transfer

Test, Revision 4 M-011-001, LGS Preventive

Maintenance

Procedure

for Diesel Generator

Heat Exchanger

Cleaning and Examination, Revision12

Standing work order R0920468-01, EDG heat exchangers

Drawings Drawing # M-109/E106214, Service Water System, Revision 50, Drawing # M-111/E106216, Emergency

Service Water System, Revision 48 Drawing # M-112/E106217, RHR Service Water System, Revision 47 Drawing # M-120/E106225, Diesel Oil Transfer System, Revision 32 SIM-M-12, Emergency

Service Water! RHR Service Water Overview, Revision 9 8031-M-11, Sh. 1-5, Emergency

Service Water, Revision 68, 81,53,50,48, respectively

8031-M-12, Sh. 1-2, Residual Heat Removal Service Water, Revision 62,6, respectively

8031-E-1045, Cathodic Protection

Plan Spray Pond & Cooling Towers Area, Revision 14 8031-E-'1046, Cathodic Protection

Plan -PCMU, RHR & ESW Piping, Units 1 & 2, Revision 14 Unit 2 RHR Heat Exchanger

Assembly & Cross Section Drawings, April 1972

Attachment

Work Orders: 796290, 796291,2E205A,889724,888029,OE505A1&2, 1078542,808322,OE505E1&2, 889732,889516,OE506A, 1111425, 1067871,OE506E,916733,889717,OE507A, 1111426, 1067872,OE507E,941280,889240

Miscellaneous

Documents

Regulatory

Guide 1.27, Ultimate Heat Sink for Nuclear Power Plants, dated January Generic Letter 89-13 and Supplement

1, Service Water System Problems

Safety-Related

Equipment, Dated July 1989 PPL responses

to GL 89-13, dated Feb. 23,1990, through Feb. 12, 1997, et al Spray Pond Inspection

Report, November 13, 2007 Zebra Mussel & Asiatic Clam Survey, November 6, 2007 ECT Test Report for Heat Exchanger

2A-E205, March 2005 WO R0966553, Clean and eddy current test 2A-E205, performed

May 19, 2005 IC-C-11-02021, Testing of Cathodic Protection

System, performed

September

4, 2007 RT-1-012-390-0, RHR Heat Exchanger

Heat Transfer Performance

Computation

Test, performed

Feb. 15, 2005 RT-2-011-251-0, ESW Loop A Flow Balance, Rev. 15, performed

April 26, 2008 RT-6-012-390-2, 2A-E205 Heat Exchanger

Heat Transfer Test, performed

Feb. 9, 2005 RT-6-109-001-0, Cathodic

Protection

Monthly Inspection, performed

September

4, 2007 ST-1-012-901-0, Spray Pond Structural

Inspection, performed

September

5,2002, August 10, 2003, August 10, 2005, and July 27,2007 ST-6-011-231-0, A Loop ESW Pump, Valve, and Flow Test, performed

May 9,2008, and August 8, 2008 ST-6-012-232-0, A Loop RHRSW Pump, Valve, and Flow Test, performed

May 16, 2008, elnd August 7,2008 Structural

Integrity

Associates, Inc., Limerick ESW/RHRSW

Pre-Outage

Support, May 7,2008 Nuclear Event Report NC-07-044, Essential

Service Water Piping Degradation, Rev. 0 & 1 Operational

Event Review -Degradation

of Essential

Service Water Piping, January 15, 2008 Technical

Evaluation

-Cumulative

Leakage from the ESW System (CR 714581-02)

Technical

Evaluation

EDG Permissible

Fouling Factors as a Function of ESW Flow and Plugged Tubes (IR 691841) Apparent Cause Evaluation -Internal

Corrosion

of RHRSW System Piping (CR 731389) Apparent Cause Evaluation -Increased

Frequency

of ESW Throttle Valve Silting (11/14/05)

Apparent Cause Evaluation

-Diesel Heat Exchanger

GL 89-13 Heat Transfer Test Performed

Too Soon After Cleaning (CR 174574) RHRSW Pipe Minimum Wall Thickness

Action Plan (IR 693495-32)

1 D-G501, EDG Heat Exchanger

Inspection

Report, June 23, 2008 2D-G501, EDG Heat Exchanger

Inspection

Report, December 10,2007 LG 96-02349-000, Undersized

Lube Oil Cooler LG 01-0'1096-000, LGS Unit 1 & 2 GL 98-13 Program Recommendation

-Heat Exchanger

Cleaning LG 01-00968-000, Final Report on DG Heat Exchanger

Performance

Tests GL 89-13 Calculation

LM-0225, Performance

Curve for EDG Heat Exchanger

for GL 89-13 Engineering

Analysis LEAM-0007, Emergency

Diesel Heat Exchanger

Performance

Tests GL 89-13, September

10, 2001. Evaluation

of 0-22 EDG Heat Exchanger

Performance

Test of August 26, 2003 Evaluation

of 0-22 EDG Heat Exchanger

Performance

Test of July 24,2004 Attachment

Evaluation

of lube oil cooler fouling factor increases

in winter, October 1, Commitment

Change Evaluation

ECR LG 96-02349, Undersized

Lube Oil ECR LG 01-01096, GL 98-13 Program Recommendation

Heat Exchanger

ECR LG 01-00968, Final Report on DG Heat Exchanger

Performance

Tests GL ECR LG 04-00433, Licensing

Basis of RHRSW Summary of RHRSW/ESW

Valve Pit

Other: Station Health Reports for RHR and EDG Systems: 2009, 1 st period -Jan 1 -May 2008, 1 51 period -Jan 1 -Apr. 2 nd period -May 1-Aug. 3 rd period -Sept 1 -Dec. 2007, 1 sl period -Jan 1 -Apr 2 nd period -May 1 Aug 3rd period Sept 1-Dec Eddy Current Testing Final Reports 1E205B** 1B RHR Hx, 2E205A -1A RHR Hx, OE505 -Ai, A2, E1, E2, OE505, OE506 A, E, OE526 E, OE507 A, E ESSW Spray Pond Dive Inspection

Report Ecology III, Inc. report dated 3 August 2009 SO-054-A03, Quarterly

ESW flow verification

-Loop A, February 23, 2005 and November 24, 2004 SO-054-803, Quarterly

ESW flow verification

-Loop B, February 16, 2005 and November 17, 2004 TP-054-076, ESW flow balance, September

24, 2004 Chemistry

Matrix Ch-054-001 (ESW), Revision 23, March 05, 2008 Design Calculations

CALC EC-CHEM-1018, Justification

for the Assurance

of Adequate Heat Removal Capabilities, Revision 5 CALC EC-054-0537, ESW System Heat Load and Flow Rate Requirements

for Updated Power Conditions, Revision 5 CALC-049-1001, RHR Heat Exchanger

Performance

at 8000 gpm RHR Flow, Revision 5 Section 1R11: Operator Re-qualification

Program Condition

Report: 1159194,1173155,1173182,622658,625137,389555,1166686

Procedures:

ON-164-002, Loss of Reactor Recirculation

Flow, Revision 28 ON-178-002, Core Flux Oscillations, Revision 14 Attachment

ON-100-101, SCRAM, SCRAM Imminent, Revision EO-000-113, Level/Power

Control, Revision EO-000-102, RPV Control, Revision NDAP-QA-0725, Operating

Experience

Review Program, Revision Other: OP002-09-06-01, Simulator

Scenario, Revision 0 Section 11R12: Maintenance

Effectiveness

Condition

Report: 1172458,1173175,1173454,1173859,1174337

Procedure:

ES-002-001, Supplying

125 VDC Loads with Portable Diesel Generator, Revision 12 Work Orders: 1172466,1172530

Section 1R13: Maintenance

Risk Assessments

and Emergent Work Control Condition 1162039,1172088,1171760,1171814, 1171764,and

MT-GE-030, ITT Damper Hydramotor

Model NH91 NH93 Overhaul, Revision OI-AD-029, Emergency

Load Control, Revision MT-GE-030, ITT Damper Hydramotor

Model NH91 and NH93 Overhaul, Revision

E-102, Sheet 17, ESS Transformer

101R201 Isolating

Relay Control, Revision 13 E-102, Sheet 17 Circuit Breaker DA10406 Control, Revision 11 M-144, Sheet 2, Reactor Water Clean-Up, Revision 11 M-144, Sheet 1, Reactor Water Clean-Up, Revision 41 E6-8, sheet 1, ESS Trans EX201 and OX203, Revision 8 VC-175, Heating, Ventilation

and Air-Conditioning

Control Diagram SBGT System, Revision 31 M-145, Sheet 1, Clean-up Filter Demineralizer, Revision 21 Work Order: 1162052 and 828214 Other: Attachment

2009 RFM Daily Status Report August 3-4,2009 -Cask 53 Section 1 R15: Operability

Evaluations

Condition

Reports: 1159448,1159214,1159461,478425,794697,478350, 1160418, 1160653, 1112465,

1147886,1145418,1152053,1152076,1161825, 1162050, 1172110, and

FSAR TRO

J-412, Sheet 6, RHR SW Pump Discharge

Pressure, Revision M-134, Sheet 3, A -D Diesel Auxiliaries

Starting Air System, Revision Work Engineering

Work

EWR 10M 183-2, KSV Diesel Generator

Instruction

Manual, Revision Section 1 R18: Permanent

Plant Modifications

Condition

1179204,1179788,1179777,1178870,1136097, 1136107, 1136188,

FSAR 9.4.2.2,9.2.12.3, Table TRO 3.8.6 and LA-1K206B-001, 1K206B Reactor Building Chiller B Safety Indicator

Panel, Revision

M310-245, Sheet 2, Chiller 1K206B, Revision Work

Attachment

Engineering

Work Request: EWR 1086364 TEC 1136133, Bypass Gas Discharge

Temperature

Trip on -IK206B Other: 10M 694, Type SL Core Form Substation

Transformer

Type UTT-B Load Tap Changer Spare Startup Transformer, Revision 2 Section '1 R19: Post-Maintenance

Testing Condition

Reports: 1079703" 1161553, 1174414, 1174403, 1177692, 1177906, 1183410 Procedures:

SO-151-014, Core Spray System Cold Shutdown Valve Exercising, September

28,2009, Revision 16 SO-151-A04, Quarterly

Core Spray Valve Exercising

Division I, September

28,2009, Revision 9 SO-152-006, High Pressure Coolant Injection

Comprehensive

Flow Verification, Revision 8 SO-158-001, "Weekly Manual Scram Control Switch Functional

Check," Revision 12 OP-003-003, Startup Bus 20 (OA104)fr20

Outage and restoration, Revision 1 Drawing 9220248, Connection

Diagram Hydraulic

Control Unit, Revision 3 10505411, Box and Cables Hydraulic

Control Unit, Revision 3 105D5634, Connection

Diagram Hydraulic

Control Unit, Revision 2 922D234, Assembly Electrical

box, Revision 3 E-157, Sheet 3, Trip Signals to hydraulic

control unit Unit 1, Revision 7

Sheet 12, Elementary

Diagram Reactor Protection

System, Revision 13 Work Orders: 1046829., 1177693, 1012176 Engineering

Work Reguest: EC 1100766, Generic ECO 480V MCC Bucket Replacement

Section'1R22:

Surveillance

Testing Condition

Reports: 10419999,1159516, 1159518,1159520,1176579,917309,1041999, 1176718,1176719

Procedures:

Attachment

SE-070-A09, "A" SGTS HEPA Filter and Charcoal Adsorber in-Place Leak Test, Revision 5 MT -GM-076, Operations

of the Aerosol Detector and Aerosol Generator

for Testing HEPA Filters, Revision 3 MT-GM-077, Operation

of the Halide Detector and Halide Generator

for Testing Charcoal Filters, Revision 4 SI-250-312, 24 Month calibration

of RCIC System Pump Flow Channel FT-E51-2N003

Remote Shutdown SE-150-004, RCIC Functional

Test at 1C2014, January 21,2008, Revision SE-100-008, RCIC Functional

test at Remote Shutdown Panel, Revision SE-200-008, RCIC Functional

test at Remote Shutdown Panel, January 21, 2009, Revision SE-100-011, HV143F023B, Functional

Test at 1C2014, March 5, 2008, Revision Work Orders: 875249,1130776

Drawing: VC-175, Sheet 3, HVAC Control Diagram RB SGTS, Revision 31 E-201, Sheet 9, SGTS Dampers HD-0755A &B, Revision 17 E-154, Sheet 3, RCIC Outboard Steam Line Isolation

Valve Unit 1, Revision 18 E-154, Sheet 22, RCIC Outboard Steam Line Isolation

Valve Unit 2, Revision 5 E-149, Sheet 6, Remote Shutdown Panel 2C201, transfer Switches Unit 2, Revision 9 Section 1 EP6 Drill Evaluation

Condition

EP-TP-001, EAL Classification

Levels, Revision August 25,2009 Drill Results Section 20S1: Access Control to Radiologically

Significant

Areas Condition

1168353; 1167515; 1167427;

1162310; and Section 20S2: ALARA Planning and Controls Condition

1155780; 1153396; and Section 20S3: Radiation

Monitoring

Instrumentation

Attachment

Quality Assurance

Internal Audit Reports: 665555; 819260; and 1093653 NIST NVLAP On-Site Assessment

Report, March 13,2009 Personnel

Dosimetry

Performance

Testing Quarterly

Report, 4th Quarter 2007 Section 40A1: Performance

Indicator

Verification

NDAP-QA-0737, Reactor Oversight

Process Performance

Indicators, Revision Operator Logs, Unit 1 and Unit Section 40A2: Identification

and Resolution

of Problems Condition

Reports: 1159518, 1159523, 1160653, 1161370, 1161398, 1162307, 1168487, 1168500, 1172365, 1173445,1173454,1174011,1174052,1174964,1175030, 1175048, 1175140, 1175332, 1175332, 1176331,1176959,1177165,1177499,1177965,1178870, 1179656, 1179995, 1027040,1044490,1073866,1114121,1128499, 1147908, 1148761,1148762,1148765, 1148790,1148824,1148828,1148834,1148851, 1148852, 1148853, 1148854, 1148859, 1148862,1148879,1148884,1148887,1148891, 1148895, 1148900,1157872,1158039, 1162998,.1173604,1173611,1173614, 1173619,1173697, 1181243 Engineering

Work Request: 1161370 Procedures:

NDAP-00-0109, "Employee

Concerns Program", Revision 13 NDAP-QA-0702, "Action Request and Condition

Report Process", Revision 23 NRC Letter-EA-09-003, Work environment

Issues at SSES-PCE, dated January 28, 2009 PPL Lettt:3r PLA-6486, SSES NRC Request to Address Work Environment

Issues at SSES, dated February 27, 2009 PPL Letter PLA-6489 SSES NRC Request to Address Work Environment

Issues at SSES, dated March 13, 2009 PPL Letter PLA-6528 SSES PPL Susquehanna

LLC Work Environment

Improvement

Plan, dated June 23, 2009 SSES Organization

chart dated 9/10/2009

SSES Concerns Hotline flyer Attachment

Safety Conscious

Work Environment

Trending Survey November 2008, Revision 0 General Work Environment-PCE

Power Point Presentation, dated June 15, 2009 Communication

Plan for Work Environment

Root Cause Analysis report, dated June 3, 2009 USNRC Allegation

Website allegation

data from January 2005 -August 2009 SSES Organizational

Effectiveness

Oversight

Panel, Employee Focus Group Meeting May 5-7, 2009 summary report SSES Focus (Internal

Communications

newsletter)

dated July 16, 2009; July 21,2009; July 29, 2009; July 31, 2009:;August

7, 2009 (2); August 14, 2009, August 17,2009, August 20, 2009, August 24,2009, August 26,2009, August 31,2009; September

1,2009, September

4, 2009; September

11, 2009; September

14, 2009 (2); September

15, 2009; September

22, 2009; and September

23, 2009 SSES Grapevine

dated August 28, 2009; September

2, 2009; and September

8, SSES Work Environment

Performance

Indicators

for July 2009 and August Proposed Draft General Work Environment

Performance

Indicator

data September

23, PPL Performance

Planning and Review Process-Personnel

Goals and Observation

sheet dated April 21, Nuclear culture review survey provided to Operations

Department

on 8/19/09 and

evaluation

of the data Memorandum

of Agreement

between PPL and IBEW Local 1600 dated may 9,2002 SSES RCA rollout Presentation

and feedback forms Section 40A5: Other Condition

Reports: 1173698 ISFSI related Condition

Reports since July 12, 2006 Procedures:

ME-ORF-023, Dry Fuel Storage 61 BT Dry Shielded Canister, Revision 14 MT -EO-045, Guidance and Use of NUHOMS Automated

Welding System for Welding Operation, Revision 1 ME-ORF*,179, Dry Fuel Storage EqUipment

List and Reference

Information, Revision 8 NDAP-QA-0658, Dry Fuel Storage Program, Revision 6 IVIE-ORF-152, Dry Fuel Storage Response to Crane/RigginglTransfer

Equipment, Malfunction

and Certificate

of Compliance

Technical

Specification

Requirements, Revision 2 MT-EO-058, E1000 Series Vacuum Drying System Operation, Revision 8 ME-ORF*,150, Dry Fuel Storage Dry Shielded Canister Unloading, Revision 1 RE-081-43, Selection

and Monitoring

of Fuel for Dry Storage, Revision 5 ON-089-001, Dry Fuel Storage Temperature

Anomaly, Revision 6 MT-199-001, Reactor Building Crane Operating

Procedure, Revision 18 MT-199-002, Reactor Building Crane Main & Auxiliary

Hoist Limit Switch Testing, Revision 6 MT-GM-014, Rigging and Lifting Equipment

Inspection, Revision 16 Work Orders: ERPM 937419, Inspect 1H213 Crane for Proper Operation

ERPM 1065158, 1H213 Perform 4 year Weld Inspections, completed

May 30,2009 Attachment

Other: 2008 PPL SSES LLC Dry Fuel Storage Project Completion

Review Self

2009 Dry Fuel Storage Readiness Annual Synthetic

Round Sling Inspection

72.48 Screens, SO 00041, SO 00035, SO 00038, SO 00033, SO 00035, SO 00028, SO 00027, SO 00024, SO 00000022, SO 00016, SO 00015, SO Final safety Analysis Report (FSAR), November 9, Decay Heat Calculation, EC-Fuel-1185, Revision FACCTAS for DSC #53, July 31,2009, Revision ISFSI Temperature

Monitoring

System Software Requirement

Specification, July 2, Revision Annual Preventative

Maintenance

Plan for Unit 1 Reactor Building Crane, WO completed

December 5, SSES Area Survey Map, ISFSI Facility, dated: January 28, 2008; April 22, 2008; 25, 2008; October 24, 2008; January 22, 2009; April 25, 2009; May 1, LIST OF ACRONYMS ADAMS Agencywide

Document and Access Management

System ALARA As Low As Is Reasonably

Achievable

AV Apparent Violation

CAP Corrective

Action Program CFR Code of Federal Regulations

CR Condition

Report DG Diesel Generator

ECP Employee Concerns Program EDG Emergency

Diesel Generator

EPU Extended Power Uprate ESW Emergency

Service Water FIN Finding FPE Fire Protection

Engineer FPPR Fire Protection

Program Report FSAR [SSES] Final Safety Analysis Report HPCI High Pressure Coolant Injection

HV High Voltage IN Information

Notice IMC Inspection

Manual Chapter ISFSI Independent

Spent Fuel Storage Installation

lSI Inservice

Inspection

IWIIISI In Vessel Visual I nspectionll

nservice Inspection

LCO Limiting Condition

for Operation

NCV Non-Cited

Violation

NDAP Nuclear Department

Administrative

Procedure

NRC Nuclear Regulatory

Commission

PARS Publicly Available

Records PCE Potential

Chilling Effect PI [NRC] Performance

Indicator

PM Preventive

Maintenance

Attachment

PMT PPL QA RCA RCIC RHR RHRSW

RTP SBO SCWE SOP SGTS

SRO SSC SSES TS T20 Post-Maintenance

Test PPL Susquehanna, LLC Quality Assurance

Root Cause Analysis Reactor Core Isolation

Cooling Residual Heat Removal Residual Heat Removal Service Water Rated Thermal Power Station Blackout Safety Conscious

Work Environment

Significance

Determination

Process Standby Gas Treatment

System Senior Reactor Operator Structures, Systems and Components

Susquehanna

Steam Electric Station Technical

Specifications

T20 Startup Transformer

Attachment