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{{#Wiki_filter:ACCELERATED DISIKBUTION DEMONSTRA.TION SYSTEMREGULATINFORMATION DISTRIBUTION+STEM (RIDE)ACCESSION NBR:8903220424 DOC.DATE:
{{#Wiki_filter:ACCELERATED DISIKBUTION DEMONSTRA.TION SYSTEM REGULAT INFORMATION DISTRIBUTION+STEM (RIDE)ACCESSION NBR:8903220424 DOC.DATE: 89/03/14 NOTARIZED:
89/03/14NOTARIZED:
NO DOCKET FACIL:50-4lg Beaver Valley Power Station, Unit 2, Duquesne Light C 05000412 AUTH.NAME AUTHOR AFFILIATION NOONANFT.P.
NODOCKETFACIL:50-4lg BeaverValleyPowerStation,Unit2,DuquesneLightC05000412AUTH.NAMEAUTHORAFFILIATION NOONANFT.P.
Duquesne Light Co.RECIP.NAME RECIPIENT AFFILIATION
DuquesneLightCo.RECIP.NAME RECIPIENT AFFILIATION


==SUBJECT:==
==SUBJECT:==
LER89-003-00:on 890212,reactor trippedduetomainfeedwater regulating valvefailure.W/890314 ltr.W/8DISTRIBUTION CODE:IE22DCOPIESRECEIVED:LTR tENCLISIZE:TITLE:50.73LicenseeEventReport(LER),IncidentRpt,etc.NOTES:LPDR 2cysTranscripts.
LER 89-003-00:on 890212,reactor tripped due to main feedwater regulating valve failure.W/890314 ltr.W/8 DISTRIBUTION CODE: IE22D COPIES RECEIVED:LTR t ENCL I SIZE: TITLE: 50.73 Licensee Event Report (LER), Incident Rpt, etc.NOTES:LPDR 2cys Transcripts.
LPDR2cysPDRDocuments.
LPDR 2cys PDR Documents.
Application forpermitrenewalfiled.05000412RECIPIENT IDCODE/NAME PDl-4LATAMFPINTERNAL:
Application for permit renewal filed.05000412 RECIPIENT ID CODE/NAME PDl-4 LA TAMFP INTERNAL: ACRS MICHELSON ACRS WYLIE AEOD/DSP/TPAB ARM/DCTS/DAB NRR/DEST/ADE 8H NRR/DEST/CEB 8H NRR/DEST/ICSB 7 NRR/DEST/MTB 9H.NRR/DEST/RSB 8E NRR/DLPQ/HFB 10 NRR/DOEA/EAB 11 NRR/DREP/RPB 10 NUDOCS-ABSTRACT RES/DSIR/EIB RGN1 FILE 01 EXTERNAL: EGSG WILLIAMSFS H ST LOBBY WARD NRC PDR NSIC MURPHYFG.A NOTES: COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 2 2 1 1 1 1 1 1 4 4 1 1 1'1 1 2 2 RECIPIENT ID CODE/NAME PD1-4 PD ACRS MOELLER AEOD/DOA AEOD/ROAB/DSP DEDRO NRR/DEST/ADS 7E NRR/DEST/ESB 8D NRR/DEST/MEB 9H NRR/DEST/PSB 8D NRR/DEST/SGB 8D NRR/DLPQ/QAB 10 NRR/DREP/RAB 10 NRRJ3/SIB 9A REG Fjj 02 RES/DSR/FRAB FORD BLDG HOYFA LPDR NSIC MAYSFG COPIES LTTR ENCL 1 1 2 2 1 1 2 2 1 1 1 0 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 NOZE'IO ALL'RIDS" RICIPZEPIS:
ACRSMICHELSON ACRSWYLIEAEOD/DSP/TPAB ARM/DCTS/DAB NRR/DEST/ADE 8HNRR/DEST/CEB 8HNRR/DEST/ICSB 7NRR/DEST/MTB 9H.NRR/DEST/RSB 8ENRR/DLPQ/HFB 10NRR/DOEA/EAB 11NRR/DREP/RPB 10NUDOCS-ABSTRACT RES/DSIR/EIB RGN1FILE01EXTERNAL:
PIZASE HELP US IO IlEDUCE%ASTl CGKPACT IHE DCjCUNE&#xc3;Z CG&#xc3;IK)L DESKF ROC'l-37 (EXT.20079)%0 EIZKBRXS YOUR MHB HKH DISTBZBUTICN LIBTS FOR DOC(IMENIS YOU DQHFT NEED<TOTAL NUMBER OF COPIES REQUIRED: LTTR 47 ENCL 46
EGSGWILLIAMSFS HSTLOBBYWARDNRCPDRNSICMURPHYFG.A NOTES:COPIESLTTRENCL111111111111111111111111112211111144111'1122RECIPIENT IDCODE/NAME PD1-4PDACRSMOELLERAEOD/DOAAEOD/ROAB/DSP DEDRONRR/DEST/ADS 7ENRR/DEST/ESB 8DNRR/DEST/MEB 9HNRR/DEST/PSB 8DNRR/DEST/SGB 8DNRR/DLPQ/QAB 10NRR/DREP/RAB 10NRRJ3/SIB9AREGFjj02RES/DSR/FRAB FORDBLDGHOYFALPDRNSICMAYSFGCOPIESLTTRENCL112211221110111111111111111111111111NOZE'IOALL'RIDS"RICIPZEPIS:
PIZASEHELPUSIOIlEDUCE%ASTlCGKPACTIHEDCjCUNE&#xc3;Z CG&#xc3;IK)LDESKFROC'l-37(EXT.20079)%0EIZKBRXSYOURMHBHKHDISTBZBUTICN LIBTSFORDOC(IMENIS YOUDQHFTNEED<TOTALNUMBEROFCOPIESREQUIRED:
LTTR47ENCL46


NRCForm388(9.83)I(LICENSEEEVENTREPORTILER)U.S.NUCLEARREGULATORY COMMISSION APPROVEOOMBNO.31504104EXPIRES:8/31/88FACILITYNAMEIIITITLE(4)ReactorTripDuetoMainFeedwater Regulating ValveFailureDOCKETNUMBER(2)05000PAGE3/1OF0FVENTDATE(5)LERNUMBER(5)REPORTDATEI7)OTHERFACILI'TIFS INVOLVED(8)MONTHOAYYEARYEARSEGVENTIAL NVMSEAyh'.REVISION'AiNUMBERMONTHOAYYEARFACILITYNAMESDOCKETNUMBER(s) 0500021289890030003489N/A05000OPERATING MODE(SIPOWERLEYELP55(10)5?'PNryr'Q?y r'rc'yvynHXrg?e"@.gp.'0.402(bl 20.405(el(I i(i)20.405(el(1)(ii)20.405(eI)II(ii))20.405(~l(l)IIv)20.405(~l(1)(vl20A05(cl50.35(cl(II 50.35IcI(2)5073(el(2)li)d0.73(~l(2)(i/I50.73(e)(2I(iii)LICENSEECONTACTFORTHISLER(12)50.73(e)(2)(iv)50.73(~)(2)(v)50,73(~)(21(viil50.73(~)(2)(wii)IAI 50.73(~)12)(wii)IBI 50.73(~)(2)(rrl0THEREOUIREMENTS OF10CFR(I:/CheckoneormorcOItncIoliowrnP/
NRC Form 388 (9.83)I(LICENSEE EVENT REPORT ILER)U.S.NUCLEAR REGULATORY COMMISSION APPROVEO OMB NO.31504104 EXPIRES: 8/31/88 F AC I LIT Y N A ME I I I TITLE (4)Reactor Trip Due to Main Feedwater Regulating Valve Failure DOCKET NUMBER (2)0 5 0 0 0 PAGE 3/1 OF 0 FVENT DATE (5)LER NUMBER (5)REPORT DATE I7)OTHER FACILI'TIFS INVOLVED (8)MONTH OAY YEAR YEAR SEGVENTIAL NVMSEA yh'.REVISION'Ai NUMBER MONTH OAY YEAR FACILITY NAMES DOCKET NUMBER(s)0 5 0 0 0 212 89 89 003 0 0 03 4 89 N/A 0 5 0 0 0 OPERATING MODE (SI POWE R LEYEL P 5 5 (10)5?'PNryr'Q?y r'rc'yvynHX rg?e"@.gp.'0.402(bl 20.405(el(I i(i)20.405(e l(1)(ii)20.405(e I)I I (ii))20.405(~l(l)I Iv)20.405(~l(1)(vl 20A05(cl 50.35(cl(II 50.35 Ic I (2)50 73(el(2)li)d0.73(~l(2)(i/I 50.73(e)(2 I (iii)LICENSEE CONTACT FOR THIS LER (12)50.73(e)(2)(iv)50.73(~)(2)(v)50,73(~)(21(viil 50.73(~)(2)(wii)IAI 50.73(~)12)(wii)IBI 50.73(~)(2)(rrl 0 THE REOUIREMENTS OF 10 CFR (I:/Check one or morc OI tnc IoliowrnP/
(11)THISREPORTISSUBMITTED PURSUANTT73.71(b)73.71IclOTHER/SpetiryInAprrreCtoe/owenriinTert,NIICForm366AINAMEMr.ThomasP.Noonan,PlantManagerTELEPHONE NUMBERAREACODE412643-125COMPLETEONELINEFOREACHCOMPONENT FAILUREOESCRIBEO INTHISREPORT(13)CAUSESYSTEMCOMPONENT MANUFAC.TURERREPORTABLE pCAUSESYSTEMCOMPONENT MANVFAC.TVRERXJBFCVC635Y$P:,"'''.'SVPPLEMEN1'AL REPORTEXPECTFD(14)YES//Iycr,comp/etcEXPECTEDSU84IISSIOIY DATE/ABSTRACTILimrtto/400rpeccr./c,,epprovimeteiy
(11)THIS REPORT IS SUBMITTED PURSUANT T 73.71(b)73.71Icl OTHER/Spetiry In AprrreCt oe/ow enriin Tert, NIIC Form 366AI NAME Mr.Thomas P.Noonan, Plant Manager TELEPHONE NUMBER AREA CODE 41 264 3-1 25 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE OESCRIBEO IN THIS REPORT (13)CAUSE SYSTEM COMPONENT MANUFAC.TURER REPORTABLE p CAUSE SYSTEM COMPONENT MANVFAC.TVRER X JB FCV C63 5 Y$P:,"'''.'SVPPLEMEN1'AL REPORT EXPECTFD (14)YES//I ycr, comp/etc EXPECTED SU84IISSIOIY DATE/ABSTRACT ILimrt to/400 rpeccr./c,, epprovimeteiy
/i/teenr/npletortetyPcwrinen
/i/teen r/nple torte tyPcwrinen
/inn/l(d)EXPECTEDSU8MISSI0NDATE(15IMONTHOAYYEARNRCForm358(983)On2/12/89,withtheUnitinPowerOperation, apowerreduction from904reactorpowerto50%reactorpowerwasinprogressaspartofEndofCoreLifeprograms.
/inn/l(d)EXPECTED SU 8 M I SS I 0 N DATE (15I MONTH OAY YEAR NRC Form 358 (9 83)On 2/12/89, with the Unit in Power Operation, a power reduction from 904 reactor power to 50%reactor power was in progress as part of End of Core Life programs.At 0048 hours, operators noticed erratic operation of the"C" Main Feedwater Regulating Valve (MFRV).The operators placed the"C" MFRV in manual to control steam generator level.At 0108 hours at approximately 55~reactor power, the"A" Main Feedwater Pump was shutdown to reduce the pressure differential across the valve allowing easier valve movement and control.At 0120 hours, a turbine trip/reactor trip occurred due to a high water level in the"C" steam generator.
At0048hours,operators noticederraticoperation ofthe"C"MainFeedwater Regulating Valve(MFRV).Theoperators placedthe"C"MFRVinmanualtocontrolsteamgenerator level.At0108hoursatapproximately 55~reactorpower,the"A"MainFeedwater Pumpwasshutdowntoreducethepressuredifferential acrossthevalveallowingeasiervalvemovementandcontrol.At0120hours,aturbinetrip/reactor tripoccurredduetoahighwaterlevelinthe"C"steamgenerator.
The operators stabilized the plant in Hot Shutdown utilizing the Emergency Operating Procedures.
Theoperators stabilized theplantinHotShutdownutilizing theEmergency Operating Procedures.
The HC" MFRV was found to have sheared anti-rotation pins and the stem detached from the valve plug.The cause for the valve failure was attributed to hydraulic forces and vibration acting over time.The MFRVs were all disassembled, inspected and repaired as necessary.
TheHC"MFRVwasfoundtohaveshearedanti-rotation pinsandthestemdetachedfromthevalveplug.Thecauseforthevalvefailurewasattributed tohydraulic forcesandvibration actingovertime.TheMFRVswerealldisassembled, inspected andrepairedasnecessary.
This event was reported to the Nuclear Regulatory Commission at 0300 hours, in accordance with 10CFR50.72.b.2.ii.
ThiseventwasreportedtotheNuclearRegulatory Commission at0300hours,inaccordance with10CFR50.72.b.2.ii.
There were no safety implications to the public as a result of this event.This type of event has previously been analyzed as stated in the Updated Final Safety Analysis Report, Section 15.1.2,"Feedwater System Malfunctions Causing an Increase In Feedwater Flow".8903220424 8903i4$)PDR ADOCK 05000412 S PNU
Therewerenosafetyimplications tothepublicasaresultofthisevent.Thistypeofeventhaspreviously beenanalyzedasstatedintheUpdatedFinalSafetyAnalysisReport,Section15.1.2,"Feedwater SystemMalfunctions CausinganIncreaseInFeedwater Flow".8903220424 8903i4$)PDRADOCK05000412SPNU


NRCForm3SSA(943)LICENSEEEENTREPORTILER)TEXTCONTINUATION U.S.NUCLEARRFOULATORY COMMISSION APPROVEDOMBNO.3150-CI04 EXPIRES:8/3)/88FACILITYNAME<<IDOCKETNUMBER)2ILERNUMBER)8)i+:SEQUENTIAL SFINUMS8rrRFVISIONNUMBERPAGE)3)BeaverValleyPowerStation,Unit2ppppp412TEXT///rrroro H>>co/rroqo/rod.
NRC Form 3SSA (943)LICENSEE E ENT REPORT ILER)TEXT CONTINUATION U.S.NUCLEAR RFOULATORY COMMISSION APPROVED OMB NO.3150-CI04 EXPIRES: 8/3)/88 FACILITY NAME<<I DOCKET NUMBER)2I LER NUMBER)8)i+: SEQUENTIAL SFI NUMS 8 rr RFVISION NUMBER PAGE)3)Beaver Valley Power Station, Unit 2 p p p p p 4 1 2 TEXT///rrroro H>>co/r roqo/rod.o>>odd/I/orM/HRC Form36548l
o>>odd/I/orM/HRC Form36548l
<<7)8 9 0 0 3 00 02 QF 0 4 DESCRIPTION On 2/12/89, with the Unit in Power Operation (Operating Mode 1), Operations personnel were reducing reactor power from 90%to 50<as part of End of Core Life programs.Prior to the Operating crew assuming the shift at 2300 hours on 2/11/89, the<<B<<Main Feedwater Regulating Valve (MFRV)had previously exhibited erratic valve control for steam generator water level.The<<B<<MFRV was in the automatic mode, however, the valve was not controlling smoothly.At 0048 hours, operators noticed erratic operation of the<<C<<MFRV.At 0108 hours, at approximately 554 power, the<<A<<Main Feedwater Pump was shutdown.At 0120 hours, the water level in the<<C<<steam generator increased to the high-high level setpoint (75%)causing.a turbine trip and feedwater isolation signal.The turbine trip caused a reactor trip, since reactor power was above the trip permissive of 49'.The feedwater isolation signal caused the following actions to occur: 1)trip of the running main feedwater pump, 2)auto-start of the auxiliary feedwater pumps, and 3)closure of the main feedwater regulating valves and bypass valves.Following the reactor trip, the operators utilized the Emergency Operating Procedures (E-0"Reactor Trip or Safety Injection<<
<<7)890030002QF04DESCRIPTION On2/12/89,withtheUnitinPowerOperation (Operating Mode1),Operations personnel werereducingreactorpowerfrom90%to50<aspartofEndofCoreLifeprograms.
and ES-0.1"Reactor Trip Response")to stabilize the plant in Hot Standby (Operating Mode 3).APPARENT CAUSE OF THE EVENT The cause for this event was attributed to the failure of the<<C<<Main.Feedwater Regulating Valve (2FHS*FCV498).
PriortotheOperating crewassumingtheshiftat2300hourson2/11/89,the<<B<<MainFeedwater Regulating Valve(MFRV)hadpreviously exhibited erraticvalvecontrolforsteamgenerator waterlevel.The<<B<<MFRVwasintheautomatic mode,however,thevalvewasnotcontrolling smoothly.
This valve is a Copes-Vulcan, Model No.D-100-160, Part No.16-FA37RG.
At0048hours,operators noticederraticoperation ofthe<<C<<MFRV.At0108hours,atapproximately 554power,the<<A<<MainFeedwater Pumpwasshutdown.
The valve failure was attributed to the hydraulic forces and vibration, which over time, mechanically excite the valve, damaging the anti-rotation cage slots, plug guides, retaining pins and valve stem.The<<B<<Main Feedwater Regulating Valve was found to have damaged anti-rotation pins.Nr)C FORM 300A IS 83)'U.S~CPCI)988-33<')09 000)0  
At0120hours,thewaterlevelinthe<<C<<steamgenerator increased tothehigh-high levelsetpoint(75%)causing.aturbinetripandfeedwater isolation signal.Theturbinetripcausedareactortrip,sincereactorpowerwasabovethetrippermissive of49'.Thefeedwater isolation signalcausedthefollowing actionstooccur:1)tripoftherunningmainfeedwater pump,2)auto-start oftheauxiliary feedwater pumps,and3)closureofthemainfeedwater regulating valvesandbypassvalves.Following thereactortrip,theoperators utilizedtheEmergency Operating Procedures (E-0"ReactorTriporSafetyInjection<<
andES-0.1"ReactorTripResponse"
)tostabilize theplantinHotStandby(Operating Mode3).APPARENTCAUSEOFTHEEVENTThecauseforthiseventwasattributed tothefailureofthe<<C<<Main.Feedwater Regulating Valve(2FHS*FCV498).
ThisvalveisaCopes-Vulcan, ModelNo.D-100-160, PartNo.16-FA37RG.
Thevalvefailurewasattributed tothehydraulic forcesandvibration, whichovertime,mechanically excitethevalve,damagingtheanti-rotation cageslots,plugguides,retaining pinsandvalvestem.The<<B<<MainFeedwater Regulating Valvewasfoundtohavedamagedanti-rotation pins.Nr)CFORM300AIS83)'U.S~CPCI)988-33<'
)09000)0  


NRCForm366A194)3)LICENSEEENTREPORT(LERITEXTCONTINUAONU.S.NUCLEARREGULATORY COMMISSION APPROVEDOMBNO.3160&)04EXPIRES:8/31/88FACILITYNAME(1)DOCKETNUMBER(2)YEARLERNUMBER(6)SEQUENTIAL
NRC Form 366A 194)3)LICENSEE ENT REPORT (LERI TEXT CONTINUA ON U.S.NUCLEAR REGULATORY COMMISSION APPROVED OMB NO.3160&)04 EXPIRES: 8/31/88 FACILITY NAME (1)DOCKET NUMBER (2)YEAR LER NUMBER (6)SEQUENTIAL
+"'2REVISIONNVM8ER):.1NUMSSRPAGE(3)BeaverValleyPowerStation,Unit2osooo41289TEXT/lfmorospinto/4rtr)o/rod, ototddr)/ono/IVRC Form3664'4/OS)0030003oF04CORRECTIVE ACTIONSThefollowing corrective actionsweretakenasaresultofthisevent:Immediate:
+"'2 REVISION NVM8ER):.1 NUMSSR PAGE (3)Beaver Valley Power Station, Unit 2 o s o o o 4 1 2 8 9 TEXT/lf moro spinto/4 rtr)o/rod, oto tddr)/ono/IVRC Form 3664'4/OS)0 0 3 0 0 03oF 0 4 CORRECTIVE ACTIONS The following corrective actions were taken as a result of this event: Immediate:
1).Operations personnel utilizedtheEmergency Operating Procedures tostabilize theplantinHotStandby.2).Themainfeedwater regulating valvesweredisassembled andinspected.
1).Operations personnel utilized the Emergency Operating Procedures to stabilize the plant in Hot Standby.2).The main feedwater regulating valves were disassembled and inspected.
Theanti-rotation pinswerereplacedonallmainfeedwater regulating valves.Long-term:
The anti-rotation pins were replaced on all main feedwater regulating valves.Long-term:
AnEngineering Memorandum hasbeengenerated requesting Engineering toidentifyanactuatorandvalvedesignwhichwilleliminate themainfeedwater regulating valveproblemsduetothehydraulic forcesandvibration whichovertime,progressively damagethevalves.2).Allthreesteamgenerators willbeinspected duringtheFirstRefueling Outageforpotent'ial looseobjects.SAFETYIMPLICATIONS Therewerenosafetyimplications tothepublicasaresultofthisevent.Thistypeofeventhaspreviously beenanalyzedasstatedintheUpdatedFinalSafetyAnalysisReport(UFSAR),Section15.1.2,"Feedwater SystemMalfunctions CausinganIncreaseinFeedwater Flow".Additionally, alltherequiredEngineered SafetyFeatures(ESF)systemcomponents actuatedasfollowsasaresultofthesteamgenerator high-high waterlevelcondition 1).Turbinetrip,causingareactortripbecausereactorpowerwasgreaterthantheP-9trippermissive, 2).Feedwater following:
An Engineering Memorandum has been generated requesting Engineering to identify an actuator and valve design which will eliminate the main feedwater regulating valve problems due to the hydraulic forces and vibration which over time, progressively damage the valves.2).All three steam generators will be inspected during the First Refueling Outage for potent'ial loose objects.SAFETY IMPLICATIONS There were no safety implications to the public as a result of this event.This type of event has previously been analyzed as stated in the Updated Final Safety Analysis Report (UFSAR), Section 15.1.2,"Feedwater System Malfunctions Causing an Increase in Feedwater Flow".Additionally, all the required Engineered Safety Features (ESF)system components actuated as follows as a result of the steam generator high-high water level condition 1).Turbine trip, causing a reactor trip because reactor power was greater than the P-9 trip permissive, 2).Feedwater following:
Isolation (FWI)signal,causingtheNRCFORM34OA(94)3)A).Tripoftherunningmainfeedwater pump,B).Automatic startoftheauxiliary feedwater pumps2FWE*P22, 23Aand23B),C).Closureofthemainfeedwater regulating valvesandbypassvalves.~V.S.CPOI)988-920-889
Isolation (FWI)signal, causing the NRC FORM 34OA (94)3)A).Trip of the running main feedwater pump, B).Automatic start of the auxiliary feedwater pumps 2FWE*P22, 23A and 23B), C).Closure of the main feedwater regulating valves and bypass valves.~V.S.CPOI)988-920-889
~OOOTO  
~OOOTO  


NRCForm388A(94)3)LICENSEEENTREPORTILER)TEXTCONTINUAONV.S.NUCLEARREGULATORY COMMISSION APPROVEDOMBNO.3)50&)04EXPIRES:8/31/88FACILITYNAME(I)DOCKETNUMBER(2)LERNUMBER(8)YEARggSEOUENTIAL PP?rNUMBER.Rrr.REvrsKINNUMBERPAGE(3)8eavergallePowerStation,Unit2osooo412TEXTIIImoroZ>>oo/4re/rr/rod, IrooEdcNane/HRC
NRC Form 388A (94)3)LICENSEE ENT REPORT ILER)TEXT CONTINUA ON V.S.NUCLEAR REGULATORY COMMISSION APPROVED OMB NO.3)50&)04 EXPIRES: 8/31/88 FACILITY NAME (I)DOCKET NUMBER (2)LER NUMBER (8)YEAR gg SEOUENTIAL PP?r NUMBER.Rrr.REvrsKIN NUMBER PAGE (3)8eaver gal le Power Station, Unit 2 o s o o o 4 1 2 TEXT III moro Z>>oo/4 re/rr/rod, Iroo EdcNane/HRC
%%dmr36849/lll)890030004OF04Inaddition, theNuclearSteamSystemSupplier(NSSS)hasevaluated theutility's engineering interpretation oftheSteamGenerator Parametric LooseObjectLicensing Report(WCAP-12101),
%%dmr 3684 9/lll)8 9 003 0 0 0 4 OF 0 4 In addition, the Nuclear Steam System Supplier (NSSS)has evaluated the utility's engineering interpretation of the Steam Generator Parametric Loose Object Licensing Report (WCAP-12101), which addressed the safety significance of the potential loose part (anti-rotation pin from 2FWS*FCV498) which could be trapped in the"C" steam generator tubesheet annulus.It was concluded that the estimated time required for the loose object to wear into a tube to the minimum allowable wall thickness, is 2.4 years.The NSSS concurred with this safety evaluation justifying continued operation of the remaining operating cycle.REPORTABI LITY This event was reported to the Nuclear Regulatory Commission at 0300 hours in accordance with 10CFR50.72.b.2.ii.
whichaddressed thesafetysignificance ofthepotential loosepart(anti-rotation pinfrom2FWS*FCV498) whichcouldbetrappedinthe"C"steamgenerator tubesheet annulus.Itwasconcluded thattheestimated timerequiredforthelooseobjecttowearintoatubetotheminimumallowable wallthickness, is2.4years.TheNSSSconcurred withthissafetyevaluation justifying continued operation oftheremaining operating cycle.REPORTABI LITYThiseventwasreportedtotheNuclearRegulatory Commission at0300hoursinaccordance with10CFR50.72.b.2.ii.
This written report is being provided in accordance with 10CFR50.73.a.2.iv, as an event involving a reactor protection system (RPS)or engineered safety fea'tures (ESF)system actuation.
Thiswrittenreportisbeingprovidedinaccordance with10CFR50.73.a.2.iv, asaneventinvolving areactorprotection system(RPS)orengineered safetyfea'tures (ESF)systemactuation.
PREVIOUS OCCURRENCES There have been no previous Licensee Event Reports issued on this type of event/equipment failure at Beaver Valley Power Station Unit 2.NRC FORM 388A l94)3)AU.S.GPOr IOSS SSB SSP I)0r)10  
PREVIOUSOCCURRENCES TherehavebeennopreviousLicenseeEventReportsissuedonthistypeofevent/equipment failureatBeaverValleyPowerStationUnit2.NRCFORM388Al94)3)AU.S.GPOrIOSSSSBSSPI)0r)10  


gled~DuquesneltNuclearGroupP,O,Box4Shippingporh PA15077~TelephOne (412)393-6000March14,1989ND3SPM:0422 BeaverValleyPowerStation,UnitNo.2DocketNo.50-412,LicenseNo.NPF-73LER89-003-00 UnitedStatesNuclearRegulatory Commission DocumentControlDeskWashington, DC20555Gentlemen:
gled~Duquesne lt Nuclear Group P,O, Box 4 Shippingporh PA 15077~TelephOne (412)393-6000 March 14, 1989 ND3SPM:0422 Beaver Valley Power Station, Unit No.2 Docket No.50-412, License No.NPF-73 LER 89-003-00 United States Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Gentlemen:
Inaccordance withAppendixA,BeaverValleyTechnical Specifications, thefollowing LicenseeEventReportissubmitted:
In accordance with Appendix A, Beaver Valley Technical Specifications, the following Licensee Event Report is submitted:
LER89-003-00, 10CFR50.73a.2.iv,"ReactorTripDuetoMainFeedwater Regulating ValveFailure".
LER 89-003-00, 10 CFR 50.73 a.2.iv,"Reactor Trip Due to Main Feedwater Regulating Valve Failure".Very truly yours, T.P.Noonan Plant Manager vhy Attachment
Verytrulyyours,T.P.NoonanPlantManagervhyAttachment


March14,1989ND3SPM'0422 PagetwoCC:Mr.WilliamT.RussellRegionalAdministrator UnitedStatesNuclearRegulatory Commission Region1475Allendale Rd.KingofPrussia,PA19406C.A.Roteck,OhioEdisonMr.PeterTam,BVPSLicensing ProjectManagerUnitedStatesNuclearRegulatory Commission Washington, DC20555J.Beall,NuclearRegulatory Commission, BVPSSeniorResidentInspector Mr.AlexTimme,CAPCONuclearProjectsCoordinator ToledoEdisonINPORecordsCenterSuite15001100Circle75ParkwayAtlanta,GA30339G.E.Muckle,FactoryMutualEngineering, Pittsburgh Mr.J.N.Steinmetz, Operating PlantProjectsManagerMidAtlanticAreaWestinghouse ElectricCorporation EnergySystemsServiceDivisionBox355Pittsburgh, PA15230AmericanNuclearInsurersc/oDottieSherman,ANILibraryTheExchangeSuite245270Farmington AvenueFarmington, CT06032Mr.RichardJanatiDepartment ofEnvironmental Resources P.O.Box206316thFloor,FultonBuilding*Harrisburg, PA17120Director, SafetyEvaluation
March 14, 1989 ND3SPM'0422 Page two CC: Mr.William T.Russell Regional Administrator United States Nuclear Regulatory Commission Region 1 475 Allendale Rd.King of Prussia, PA 19406 C.A.Roteck, Ohio Edison Mr.Peter Tam, BVPS Licensing Project Manager United States Nuclear Regulatory Commission Washington, DC 20555 J.Beall, Nuclear Regulatory Commission, BVPS Senior Resident Inspector Mr.Alex Timme, CAPCO Nuclear Projects Coordinator Toledo Edison INPO Records Center Suite 1500 1100 Circle 75 Parkway Atlanta, GA 30339 G.E.Muckle, Factory Mutual Engineering, Pittsburgh Mr.J.N.Steinmetz, Operating Plant Projects Manager Mid Atlantic Area Westinghouse Electric Corporation Energy Systems Service Division Box 355 Pittsburgh, PA 15230 American Nuclear Insurers c/o Dottie Sherman, ANI Library The Exchange Suite 245 270 Farmington Avenue Farmington, CT 06032 Mr.Richard Janati Department of Environmental Resources P.O.Box 2063 16th Floor, Fulton Building*Harrisburg, PA 17120 Director, Safety Evaluation
&ControlVirginiaElectric6PowerCo.P.O.Box26666OneJamesRiverPlazaRichmond, VA23261
&Control Virginia Electric 6 Power Co.P.O.Box 26666 One James River Plaza Richmond, VA 23261
,/}}
,/}}

Revision as of 02:53, 6 July 2018

LER 89-003-00:on 890212,noticed Erratic Operation of Main Feedwater Regulating Valve C & Turbine Trip/Reactor Trip Occurred Due to High Water Level in Steam Generator C.Caused by Valve Vibration & Hydraulic forces.W/890314 Ltr
ML18041A188
Person / Time
Site: Beaver Valley
Issue date: 03/14/1989
From: NOONAN T P
DUQUESNE LIGHT CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
LER-89-003, LER-89-3, ND3SPM:0422, ND3SPM:422, NUDOCS 8903220424
Download: ML18041A188 (14)


Text

ACCELERATED DISIKBUTION DEMONSTRA.TION SYSTEM REGULAT INFORMATION DISTRIBUTION+STEM (RIDE)ACCESSION NBR:8903220424 DOC.DATE: 89/03/14 NOTARIZED:

NO DOCKET FACIL:50-4lg Beaver Valley Power Station, Unit 2, Duquesne Light C 05000412 AUTH.NAME AUTHOR AFFILIATION NOONANFT.P.

Duquesne Light Co.RECIP.NAME RECIPIENT AFFILIATION

SUBJECT:

LER 89-003-00:on 890212,reactor tripped due to main feedwater regulating valve failure.W/890314 ltr.W/8 DISTRIBUTION CODE: IE22D COPIES RECEIVED:LTR t ENCL I SIZE: TITLE: 50.73 Licensee Event Report (LER), Incident Rpt, etc.NOTES:LPDR 2cys Transcripts.

LPDR 2cys PDR Documents.

Application for permit renewal filed.05000412 RECIPIENT ID CODE/NAME PDl-4 LA TAMFP INTERNAL: ACRS MICHELSON ACRS WYLIE AEOD/DSP/TPAB ARM/DCTS/DAB NRR/DEST/ADE 8H NRR/DEST/CEB 8H NRR/DEST/ICSB 7 NRR/DEST/MTB 9H.NRR/DEST/RSB 8E NRR/DLPQ/HFB 10 NRR/DOEA/EAB 11 NRR/DREP/RPB 10 NUDOCS-ABSTRACT RES/DSIR/EIB RGN1 FILE 01 EXTERNAL: EGSG WILLIAMSFS H ST LOBBY WARD NRC PDR NSIC MURPHYFG.A NOTES: COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 2 2 1 1 1 1 1 1 4 4 1 1 1'1 1 2 2 RECIPIENT ID CODE/NAME PD1-4 PD ACRS MOELLER AEOD/DOA AEOD/ROAB/DSP DEDRO NRR/DEST/ADS 7E NRR/DEST/ESB 8D NRR/DEST/MEB 9H NRR/DEST/PSB 8D NRR/DEST/SGB 8D NRR/DLPQ/QAB 10 NRR/DREP/RAB 10 NRRJ3/SIB 9A REG Fjj 02 RES/DSR/FRAB FORD BLDG HOYFA LPDR NSIC MAYSFG COPIES LTTR ENCL 1 1 2 2 1 1 2 2 1 1 1 0 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 NOZE'IO ALL'RIDS" RICIPZEPIS:

PIZASE HELP US IO IlEDUCE%ASTl CGKPACT IHE DCjCUNEÃZ CGÃIK)L DESKF ROC'l-37 (EXT.20079)%0 EIZKBRXS YOUR MHB HKH DISTBZBUTICN LIBTS FOR DOC(IMENIS YOU DQHFT NEED<TOTAL NUMBER OF COPIES REQUIRED: LTTR 47 ENCL 46

NRC Form 388 (9.83)I(LICENSEE EVENT REPORT ILER)U.S.NUCLEAR REGULATORY COMMISSION APPROVEO OMB NO.31504104 EXPIRES: 8/31/88 F AC I LIT Y N A ME I I I TITLE (4)Reactor Trip Due to Main Feedwater Regulating Valve Failure DOCKET NUMBER (2)0 5 0 0 0 PAGE 3/1 OF 0 FVENT DATE (5)LER NUMBER (5)REPORT DATE I7)OTHER FACILI'TIFS INVOLVED (8)MONTH OAY YEAR YEAR SEGVENTIAL NVMSEA yh'.REVISION'Ai NUMBER MONTH OAY YEAR FACILITY NAMES DOCKET NUMBER(s)0 5 0 0 0 212 89 89 003 0 0 03 4 89 N/A 0 5 0 0 0 OPERATING MODE (SI POWE R LEYEL P 5 5 (10)5?'PNryr'Q?y r'rc'yvynHX rg?e"@.gp.'0.402(bl 20.405(el(I i(i)20.405(e l(1)(ii)20.405(e I)I I (ii))20.405(~l(l)I Iv)20.405(~l(1)(vl 20A05(cl 50.35(cl(II 50.35 Ic I (2)50 73(el(2)li)d0.73(~l(2)(i/I 50.73(e)(2 I (iii)LICENSEE CONTACT FOR THIS LER (12)50.73(e)(2)(iv)50.73(~)(2)(v)50,73(~)(21(viil 50.73(~)(2)(wii)IAI 50.73(~)12)(wii)IBI 50.73(~)(2)(rrl 0 THE REOUIREMENTS OF 10 CFR (I:/Check one or morc OI tnc IoliowrnP/

(11)THIS REPORT IS SUBMITTED PURSUANT T 73.71(b)73.71Icl OTHER/Spetiry In AprrreCt oe/ow enriin Tert, NIIC Form 366AI NAME Mr.Thomas P.Noonan, Plant Manager TELEPHONE NUMBER AREA CODE 41 264 3-1 25 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE OESCRIBEO IN THIS REPORT (13)CAUSE SYSTEM COMPONENT MANUFAC.TURER REPORTABLE p CAUSE SYSTEM COMPONENT MANVFAC.TVRER X JB FCV C63 5 Y$P:,".'SVPPLEMEN1'AL REPORT EXPECTFD (14)YES//I ycr, comp/etc EXPECTED SU84IISSIOIY DATE/ABSTRACT ILimrt to/400 rpeccr./c,, epprovimeteiy

/i/teen r/nple torte tyPcwrinen

/inn/l(d)EXPECTED SU 8 M I SS I 0 N DATE (15I MONTH OAY YEAR NRC Form 358 (9 83)On 2/12/89, with the Unit in Power Operation, a power reduction from 904 reactor power to 50%reactor power was in progress as part of End of Core Life programs.At 0048 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br />, operators noticed erratic operation of the"C" Main Feedwater Regulating Valve (MFRV).The operators placed the"C" MFRV in manual to control steam generator level.At 0108 hours0.00125 days <br />0.03 hours <br />1.785714e-4 weeks <br />4.1094e-5 months <br /> at approximately 55~reactor power, the"A" Main Feedwater Pump was shutdown to reduce the pressure differential across the valve allowing easier valve movement and control.At 0120 hours0.00139 days <br />0.0333 hours <br />1.984127e-4 weeks <br />4.566e-5 months <br />, a turbine trip/reactor trip occurred due to a high water level in the"C" steam generator.

The operators stabilized the plant in Hot Shutdown utilizing the Emergency Operating Procedures.

The HC" MFRV was found to have sheared anti-rotation pins and the stem detached from the valve plug.The cause for the valve failure was attributed to hydraulic forces and vibration acting over time.The MFRVs were all disassembled, inspected and repaired as necessary.

This event was reported to the Nuclear Regulatory Commission at 0300 hours0.00347 days <br />0.0833 hours <br />4.960317e-4 weeks <br />1.1415e-4 months <br />, in accordance with 10CFR50.72.b.2.ii.

There were no safety implications to the public as a result of this event.This type of event has previously been analyzed as stated in the Updated Final Safety Analysis Report, Section 15.1.2,"Feedwater System Malfunctions Causing an Increase In Feedwater Flow".8903220424 8903i4$)PDR ADOCK 05000412 S PNU

NRC Form 3SSA (943)LICENSEE E ENT REPORT ILER)TEXT CONTINUATION U.S.NUCLEAR RFOULATORY COMMISSION APPROVED OMB NO.3150-CI04 EXPIRES: 8/3)/88 FACILITY NAME<>co/r roqo/rod.o>>odd/I/orM/HRC Form36548l

<<7)8 9 0 0 3 00 02 QF 0 4 DESCRIPTION On 2/12/89, with the Unit in Power Operation (Operating Mode 1), Operations personnel were reducing reactor power from 90%to 50<as part of End of Core Life programs.Prior to the Operating crew assuming the shift at 2300 hours0.0266 days <br />0.639 hours <br />0.0038 weeks <br />8.7515e-4 months <br /> on 2/11/89, the<<B<<Main Feedwater Regulating Valve (MFRV)had previously exhibited erratic valve control for steam generator water level.The<<B<<MFRV was in the automatic mode, however, the valve was not controlling smoothly.At 0048 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br />, operators noticed erratic operation of the<<C<<MFRV.At 0108 hours0.00125 days <br />0.03 hours <br />1.785714e-4 weeks <br />4.1094e-5 months <br />, at approximately 554 power, the<<A<<Main Feedwater Pump was shutdown.At 0120 hours0.00139 days <br />0.0333 hours <br />1.984127e-4 weeks <br />4.566e-5 months <br />, the water level in the<<C<<steam generator increased to the high-high level setpoint (75%)causing.a turbine trip and feedwater isolation signal.The turbine trip caused a reactor trip, since reactor power was above the trip permissive of 49'.The feedwater isolation signal caused the following actions to occur: 1)trip of the running main feedwater pump, 2)auto-start of the auxiliary feedwater pumps, and 3)closure of the main feedwater regulating valves and bypass valves.Following the reactor trip, the operators utilized the Emergency Operating Procedures (E-0"Reactor Trip or Safety Injection<<

and ES-0.1"Reactor Trip Response")to stabilize the plant in Hot Standby (Operating Mode 3).APPARENT CAUSE OF THE EVENT The cause for this event was attributed to the failure of the<<C<<Main.Feedwater Regulating Valve (2FHS*FCV498).

This valve is a Copes-Vulcan, Model No.D-100-160, Part No.16-FA37RG.

The valve failure was attributed to the hydraulic forces and vibration, which over time, mechanically excite the valve, damaging the anti-rotation cage slots, plug guides, retaining pins and valve stem.The<<B<<Main Feedwater Regulating Valve was found to have damaged anti-rotation pins.Nr)C FORM 300A IS 83)'U.S~CPCI)988-33<')09 000)0

NRC Form 366A 194)3)LICENSEE ENT REPORT (LERI TEXT CONTINUA ON U.S.NUCLEAR REGULATORY COMMISSION APPROVED OMB NO.3160&)04 EXPIRES: 8/31/88 FACILITY NAME (1)DOCKET NUMBER (2)YEAR LER NUMBER (6)SEQUENTIAL

+"'2 REVISION NVM8ER):.1 NUMSSR PAGE (3)Beaver Valley Power Station, Unit 2 o s o o o 4 1 2 8 9 TEXT/lf moro spinto/4 rtr)o/rod, oto tddr)/ono/IVRC Form 3664'4/OS)0 0 3 0 0 03oF 0 4 CORRECTIVE ACTIONS The following corrective actions were taken as a result of this event: Immediate:

1).Operations personnel utilized the Emergency Operating Procedures to stabilize the plant in Hot Standby.2).The main feedwater regulating valves were disassembled and inspected.

The anti-rotation pins were replaced on all main feedwater regulating valves.Long-term:

An Engineering Memorandum has been generated requesting Engineering to identify an actuator and valve design which will eliminate the main feedwater regulating valve problems due to the hydraulic forces and vibration which over time, progressively damage the valves.2).All three steam generators will be inspected during the First Refueling Outage for potent'ial loose objects.SAFETY IMPLICATIONS There were no safety implications to the public as a result of this event.This type of event has previously been analyzed as stated in the Updated Final Safety Analysis Report (UFSAR), Section 15.1.2,"Feedwater System Malfunctions Causing an Increase in Feedwater Flow".Additionally, all the required Engineered Safety Features (ESF)system components actuated as follows as a result of the steam generator high-high water level condition 1).Turbine trip, causing a reactor trip because reactor power was greater than the P-9 trip permissive, 2).Feedwater following:

Isolation (FWI)signal, causing the NRC FORM 34OA (94)3)A).Trip of the running main feedwater pump, B).Automatic start of the auxiliary feedwater pumps 2FWE*P22, 23A and 23B), C).Closure of the main feedwater regulating valves and bypass valves.~V.S.CPOI)988-920-889

~OOOTO

NRC Form 388A (94)3)LICENSEE ENT REPORT ILER)TEXT CONTINUA ON V.S.NUCLEAR REGULATORY COMMISSION APPROVED OMB NO.3)50&)04 EXPIRES: 8/31/88 FACILITY NAME (I)DOCKET NUMBER (2)LER NUMBER (8)YEAR gg SEOUENTIAL PP?r NUMBER.Rrr.REvrsKIN NUMBER PAGE (3)8eaver gal le Power Station, Unit 2 o s o o o 4 1 2 TEXT III moro Z>>oo/4 re/rr/rod, Iroo EdcNane/HRC

%%dmr 3684 9/lll)8 9 003 0 0 0 4 OF 0 4 In addition, the Nuclear Steam System Supplier (NSSS)has evaluated the utility's engineering interpretation of the Steam Generator Parametric Loose Object Licensing Report (WCAP-12101), which addressed the safety significance of the potential loose part (anti-rotation pin from 2FWS*FCV498) which could be trapped in the"C" steam generator tubesheet annulus.It was concluded that the estimated time required for the loose object to wear into a tube to the minimum allowable wall thickness, is 2.4 years.The NSSS concurred with this safety evaluation justifying continued operation of the remaining operating cycle.REPORTABI LITY This event was reported to the Nuclear Regulatory Commission at 0300 hours0.00347 days <br />0.0833 hours <br />4.960317e-4 weeks <br />1.1415e-4 months <br /> in accordance with 10CFR50.72.b.2.ii.

This written report is being provided in accordance with 10CFR50.73.a.2.iv, as an event involving a reactor protection system (RPS)or engineered safety fea'tures (ESF)system actuation.

PREVIOUS OCCURRENCES There have been no previous Licensee Event Reports issued on this type of event/equipment failure at Beaver Valley Power Station Unit 2.NRC FORM 388A l94)3)AU.S.GPOr IOSS SSB SSP I)0r)10

gled~Duquesne lt Nuclear Group P,O, Box 4 Shippingporh PA 15077~TelephOne (412)393-6000 March 14, 1989 ND3SPM:0422 Beaver Valley Power Station, Unit No.2 Docket No.50-412, License No.NPF-73 LER 89-003-00 United States Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Gentlemen:

In accordance with Appendix A, Beaver Valley Technical Specifications, the following Licensee Event Report is submitted:

LER 89-003-00, 10 CFR 50.73 a.2.iv,"Reactor Trip Due to Main Feedwater Regulating Valve Failure".Very truly yours, T.P.Noonan Plant Manager vhy Attachment

March 14, 1989 ND3SPM'0422 Page two CC: Mr.William T.Russell Regional Administrator United States Nuclear Regulatory Commission Region 1 475 Allendale Rd.King of Prussia, PA 19406 C.A.Roteck, Ohio Edison Mr.Peter Tam, BVPS Licensing Project Manager United States Nuclear Regulatory Commission Washington, DC 20555 J.Beall, Nuclear Regulatory Commission, BVPS Senior Resident Inspector Mr.Alex Timme, CAPCO Nuclear Projects Coordinator Toledo Edison INPO Records Center Suite 1500 1100 Circle 75 Parkway Atlanta, GA 30339 G.E.Muckle, Factory Mutual Engineering, Pittsburgh Mr.J.N.Steinmetz, Operating Plant Projects Manager Mid Atlantic Area Westinghouse Electric Corporation Energy Systems Service Division Box 355 Pittsburgh, PA 15230 American Nuclear Insurers c/o Dottie Sherman, ANI Library The Exchange Suite 245 270 Farmington Avenue Farmington, CT 06032 Mr.Richard Janati Department of Environmental Resources P.O.Box 2063 16th Floor, Fulton Building*Harrisburg, PA 17120 Director, Safety Evaluation

&Control Virginia Electric 6 Power Co.P.O.Box 26666 One James River Plaza Richmond, VA 23261

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