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{{Adams | |||
| number = ML20148F944 | |||
| issue date = 05/23/1997 | |||
| title = Insp Repts 50-413/97-07 & 50-414/97-07 on 970323-0426. Violations Noted.Major Areas Inspected:Licensee Operations, Maint,Engineering & Plant Support | |||
| author name = | |||
| author affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) | |||
| addressee name = | |||
| addressee affiliation = | |||
| docket = 05000413, 05000414 | |||
| license number = | |||
| contact person = | |||
| document report number = 50-413-97-07, 50-413-97-7, 50-414-97-07, 50-414-97-7, NUDOCS 9706050102 | |||
| package number = ML20148F917 | |||
| document type = INSPECTION REPORT, NRC-GENERATED, TEXT-INSPECTION & AUDIT & I&E CIRCULARS | |||
| page count = 50 | |||
}} | |||
See also: [[see also::IR 05000413/1997007]] | |||
=Text= | |||
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! U.S. NUCLEAR REGULATORY COMMISSION | |||
REGION II | |||
Docket Nos: 50-413, 50-414 | |||
License Nos: NPF-35 NPF-52 | |||
Report Nos.: 50-413/97-07. 50-414/97-07 | |||
i | |||
Licensee: Duke Power Company | |||
Facility: Catawba Nuclear Station Units 1 and 2 | |||
Location. 422 South Church Street | |||
Charlotte. NC 28242 | |||
Dates: March 23 - April 26,1997 | |||
Inspectors: R. J. Freudenberger, Senior Resident Inspector | |||
P. A. Balmain, Resident Inspector | |||
R. L. Franovich. Resident Inspector | |||
. | |||
R. A. Gibbs, Resident Inspector (In Training) | |||
J. L. Coley, Jr. . Reactor Inspector (Sections M2, E2.1) | |||
D. B. Forbes, Radiation Specialist (Sections R1, R5, R7) | |||
W. H. Miller, Jr.. Reactor Inspector (Sections 08.1, F2, | |||
F3. FS, F6. F7 F8) | |||
R. L. Moore, Reactor Inspector (Sections E2.2, E4.1, E8.1. | |||
E8.2) | |||
Approved by: C. A. Casto, Chief | |||
Reactor Projects Branch 1 | |||
Division of Reactor Projects | |||
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1 | |||
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Enclosure 2 | |||
9706050102 970523 | |||
PDR ADOCK 05000413 | |||
G PDR : | |||
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EXECUTIVE SUMMARY | |||
Catawba Nucleer Station. Units 1 & 2 4 | |||
NRC Inspection Report 50-413/97-07. 50-414/97-07 ' | |||
This integrated inspection included aspects of licensee operations. ! | |||
maintenance, engineering, and plant support. The report covers a 6-week | |||
period of resident ins)ection: in addition. it includes the results of | |||
announced inspections ay regional reactor safety inspectors. l | |||
Operations | |||
. A Unit 2 loss of spent fuel pool cooling, which was caused by an | |||
inadequate containment penetration test procedure, was identified as a | |||
violation. Other barriers that could have prevented the event included l | |||
increased emphasis on the importance of the system function during the l | |||
pre-job brief and more diligent control board monitoring. The | |||
operator's performance in response to the event was appropriate. The l | |||
Catawba Safety Review Group evaluation of the event was detailed and I | |||
identified substantive corrective actions. (Section 01.1) | |||
* Midloop Activities were well controlled. Nevertheless, the process for | |||
restoring equipment necessary for gravity flows to the core may not be | |||
ensured by administrative controls. (Section 01.2) | |||
. | |||
. The inspector concluded that selected initial conditions for the | |||
compensatory action associated with the main control room pressure i | |||
boundary were satisfied. The inspector further concluded that operator | |||
effectiveness in im)lementing this complex compensatory action was I | |||
challenged by lengtly initial conditions, and the practice of not ' | |||
periodically reverifying required initial conditions. (Section 01.3) | |||
i | |||
. Problems encountered with the Boron Dilution Mitigation System during | |||
the Unit 2 refueling outage were indicative of historically low | |||
reliability and availability, which caused additional control room | |||
operator workload to compensate for the system's low reliability. | |||
(Section 01.4) | |||
. The inspector concluded that actions by operations and Radiation | |||
Protection personnel in response to the radiation alarm in the fuel | |||
handling building were good. However. foreign material exclusion | |||
' | |||
administrative controls were not properly im)lemented by personnel | |||
working in the fuel transfer canal area of t1e fuel handling building. | |||
(Section 01.5) | |||
! | |||
. A Unit 1 pressurizer )ower operated relief block valve control circuit | |||
failure occurred whic1 is a potential repeat of a previous 1995 failure. | |||
The licensee has planned appropriate actions to determine the cause of | |||
the control circuit component failure. (Section 01.6) | |||
Enclosure 2 | |||
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. _ _ _ | |||
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. | |||
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2 | |||
Maintenance | |||
. The inspector concluded that, in general, outage-related maintenance | |||
activities were ap]ropriately conducted. Although multiple barriers to | |||
minimizing the risc of human error during reactor coolant pump seal | |||
maintenance were noted, the inspector was unaware of any human | |||
performance problems associated with the work. (Section M1.1) | |||
. The licensee's resolution of long-standing elevated vibration levels | |||
associated with the Unit 2B nuclear service water pump motor was very | |||
good. Deficiencies identified with a spare nuclear service water pump | |||
motor, a previous motor failure, and findings identified by licensee | |||
assessments of warehouse storage and handling practices raised questions | |||
about control and storage of spare motors. The issue is identified as | |||
an Inspector Followup Item and will be reviewed during a future | |||
inspection. (Section M1.2) | |||
* Certification records for nondestructive examination (NDE) personnel, | |||
weld examinations, and NDE examination procedures were in accordance | |||
with Code requirements. (Section M2.1) | |||
. * Review of the eddy current outage plan, equipment setup and acquisition | |||
procedures, personnel and equipment certifications, and observation of | |||
data acquisition activities revealed that required documentation was | |||
available and complete, and data acquisition personnel were | |||
- | |||
knowledgeable of the eddy current examination process. (Section M2.2) | |||
+ The licensee has implemented an effective program for the detection of | |||
flow accelerated corrosion in components. This program is based on | |||
recommendations found in recognized industry standards. (Section M2.3) | |||
. The maintenance / work control self-assessment programs effectively | |||
identified areas for improvement and a]propriate corrective actions. | |||
The self-assessments apparently contri)uted to improvement in the | |||
performance of the Maintenance and Work Control organizations. (Section | |||
M7.1) | |||
Enaineerina | |||
. The licensee's actions to replace all control rod assemblies that had | |||
evidence of tip cracking were appropriate. (Section El.1) | |||
* Documentation for the modification of the Unit 2 pressurizer manway was | |||
satisfactory, and engineering considerations for the modification, | |||
inspection, and cleaning of the pressurizer were very good. (Section | |||
E2.1) | |||
* Design controls for Unit 2 outage modifications were consistent with | |||
regulatory requirements. (Section E2.2) | |||
Enclosure 2 | |||
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.- . -- - - - . . _ - - - - . ~ - - - . - - - - . - . . . | |||
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3 | |||
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. The motor shaft key way cracking in large high speed limitorque motor | |||
actuators at-Catawba was an example of good identification and ; | |||
I | |||
' | |||
resolution of equipment problems using the Operating Experience Program. ' | |||
(Section E4.1) | |||
L Plant Sucoort | |||
. The licensee was effectively maintaining controls for personnel . | |||
monitoring, control of radioactive material, radiological postings. and J | |||
radiation area /high radiation area controls as required by 10 CFR Part i | |||
20. One Non-Cited Violation was identified for failure to source check | |||
' | |||
l survey instruments as required by licensee procedure. (Section R1.1) | |||
[ . The licensee was maintaining programs for controlling exposures As Low I | |||
' | |||
As Reasonably Achievable and continued to be effective in controlling ' | |||
l overall collective dose. (Section R1.2) | |||
. Radiation protection technicians and radiation workers were receiving an | |||
i | |||
' | |||
appropriate level of training to perform work activities involving ) | |||
radiation and/or radioactive material. (Section RS) | |||
L . The licensee was performing Quality Assurance Audits and effectively | |||
:. assessing the radiation protection program as required by 10 CFR Part | |||
20.1101 and completing corrective actions in a timely manner. (Section | |||
l R7) | |||
l. . The low number of open maintenance work orders and degraded fire | |||
protection components, in conjunction with the good material condition | |||
i | |||
of the fire protection components and fire brigade equipment, indicated | |||
; that, in general appropriate em3hasis had been placed on the | |||
l maintenance and operability of t1e fire protection equipment and | |||
! | |||
components. (Section F2.1) | |||
' | |||
.- The work to repair the suction screens for the fire pumps' suction | |||
piping had been ooen since 1991 and was not complete. The failure to. | |||
complete this work in a timely manner was identified as a Violation. | |||
(Section F2.1) | |||
. Good surveillance and test procedures were provided for the fire | |||
protection systems and features with effective procedure implementation. | |||
.The coordination of the fire protection water piping cleaning project | |||
was excellent. (Section F2.2) | |||
! . The fire protection program implementing procedures were good and met | |||
licensee and NRC requirements. Implementation of procedures for the i' | |||
control of. ignition sources, transient combustibles, and general | |||
housekeeping was good. An issue regarding time limits for restoration ; | |||
. of inoperable fire protection components will be reviewed further by the ' | |||
l4 | |||
NRC under an Inspector Followup Item. (Section F3) | |||
: | |||
Enclosure 2 | |||
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- - - - -- . - , . . ._ -. - . . .- | |||
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! 4 | |||
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. | |||
The fire brigade organization and training met the requirements of the | |||
site procedures. Performance by the fire brigade during a drill was | |||
excellent. The use of the fire brigade safety officer position used | |||
during fire emergencies was identified as a program strength. (Section | |||
F5) | |||
l . | |||
Strong coordination and oversight were provided over the facility's fire | |||
protection program. The Fire Protection BEST was a positive force in | |||
the identification of potential problems and in the development and | |||
l implementation of enhancements to the fire protection program. (Section | |||
, | |||
F6) | |||
! | |||
. | |||
The 1995 audit and assessment of the facility's fire protection program | |||
was comprehensive and appropriate corrective action was promptly taken | |||
to reso:ve the identified issues. An issue regarding the control of OA | |||
audit frequencies was identified as an Inspector Followup Item will be | |||
reviewed further by the NRC. (Section F7) | |||
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Enclosure 2 | |||
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Report Details | |||
Summary of Plant Status | |||
Unit 1 began the ]eriod operating at 100% power and operated at essentially | |||
full power througacut the inspection period. | |||
Unit 2 began the period in cold shutdown (Mode 5) in preparation for the End | |||
of Cycle (EOC8) refueling outage. One scheduled period of reactor coolant | |||
system reduced inventory /midloop began and completed on April 23. Midloop was | |||
entered to support the reactor coolant system vacuum refill evolution. At the | |||
close of the inspection period the Unit had returned to cold shutdown (Mode 5) ! | |||
and heatup activities in preparation for unit restart were beginning. | |||
Review of Uodated Final Safety Analysis Reoort (UFSAR) Commitgents | |||
While performing inspections discussed in this report, the inspectors reviewed | |||
the applicable portions of the UFSAR that were related to the areas inspected. l | |||
The inspectors verified that the UFSAR wording was consistent with the i | |||
observed plant practices, procedures, and/or parameters, i | |||
I. Operations | |||
01 Conduct of Operations | |||
- | |||
i | |||
01.1 Loss of Spent Fuel Pool Coolina | |||
a. Insoection Scope (71707) | |||
On April 8. Unit 2 was in a refueling outage with all of the fuel off- | |||
loaded to the spent fuel pool. The Operator Aid Computer was out of ' | |||
service for replacement, and alignments for testing of containment | |||
isolation valves in the component cooling water non-essential header | |||
were in progress. Inventory was inadvertently drained from the | |||
component cooling water system over a seventy minute period. until the | |||
low-low level setpoint in the component cooling water surge tanks was | |||
reached. At this level, automatic isolation of the non-essential header | |||
occurred. the drain path was isolated, and cooling flow to the spent | |||
fuel pool heat exchanger and pump motor cooler was isolated. 0]erators | |||
shutdown the pump to prevent overheating, initiated makeup to t1e | |||
component cooling water surge tanks. and closely monitored spent fuel | |||
pool temperature. Spent fuel pool temperature increased to a maximum of | |||
108 F. within the TS limit. while operators determined the cause of the | |||
loss of component cooling water inventory and returned the non-essential | |||
l | |||
header to service. | |||
! | |||
As a result of the event, the licensee initiated Problem Investigation | |||
Process (PIP) report 2-C97-1090 and initiated a root cause evaluation | |||
that was performed by the Catawba Safety Review Group. | |||
The inspector responded to the site upon notification of the loss of | |||
spent fuel pool cooling: discussed the event with various personnel | |||
Enclosure 2 | |||
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involved; reviewed PT/2/A/4200/01T, Containment Penetration Valve | |||
Injection Water System Performance Test, approved 3/26/97: reviewed data | |||
on component cooling water surge tank level spent fuel pool cooling | |||
pump motor temperatures, and spent fuel pool temperature: and reviewed | |||
the root cause evaluation documented in the referenced PIP. | |||
b. Observations and Findinas | |||
At the time of the loss of spent fuel pool cooling, approximately 19 - | |||
hours were available prior to boiling in the spent fuel pool. Operators I | |||
methodically restored cooling within 1.5 hours, after identifying the | |||
cause, assessing equipment condition, and realigning the component . | |||
cooling water system. l | |||
The licensee's root cause evaluation considered procedural adequacy. | |||
o]erator performance, ad supervisory oversight of the evolution. In | |||
taese areas, problems were identified and appropriate corrective actions | |||
were delineated. | |||
Procedure PT/2/A/4200/01T, Containment Penetration Valve Injection Water | |||
System Performance Test, included steps for the alignment of four | |||
component cooling water containment penetrations that included valve | |||
. | |||
manipulation sequences that were incorrect. The incorrect sequences | |||
caused drain paths to be aligned through the inside containment | |||
penetration vent on all four penetrations. The licensee's evaluation | |||
revealed that the Unit 1 procedure had similar errors. The errors | |||
occurred during a process to convert engineering test procedures into | |||
the operations procedure format. Proposed corrective actions included a | |||
formal validation of the technical adequacy of other procedures that | |||
have been or were to be converted. This procedure inadequacy, which | |||
caused the loss of spent fuel cooling constitutes a Violation (VIO) of | |||
TS 6.8.1. Procedures and Programs, and is identified as VIO 50-414/97- | |||
07-01: Inadequate Procedure Resulting in Loss of Spent Fuel Pool | |||
Cooling with Core Off-loaded. | |||
The licensee's evaluation of operator performance concluded that the | |||
equipment operator that performed the valve alignments appropriately | |||
questioned the high flow rate from the vent valves as they were opened, | |||
but failed to stop and contact su3ervision when this unexpected response | |||
was obtained. Also, the control aoard operators were not timely in | |||
their assessment of an observed increased rate of input to the | |||
containment floor and equipment sump. | |||
The inspector noted that the pre-job brief for performing the | |||
containment Jenetration alignments was incomplete. Personnel conducting | |||
the pre-job arief did not emphasize that the component cooling water | |||
i | |||
system was affected by the procedure and was being relied upon for | |||
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Enclosure 2 | |||
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cooling the spent fuel pool with the core off-loaded. Also, the control | |||
room operators could have more diligently monitored this system, since | |||
it was performing an important function, and identified the decreasing | |||
level in the component cooling water surge tanks before automatic | |||
, actions occurred. Operations management had similar observations and | |||
l took actions to imarove monitoring of systems performing important | |||
functions during t1e remainder of the outage. | |||
c. Conclusions | |||
; | |||
l The loss of spent fuel pool cooling was caused by an inadequate ; | |||
i | |||
containment penetration test procedure. Other barriers that could have | |||
l | |||
! | |||
prevented the event included increased emphasis on the importance of the | |||
system function during the pre-job brief and more diligent control board | |||
monitoring. The operator's performance in response to the event was | |||
appropriate. The Catawba Safety Review Group evaluation of the event | |||
was detailed and identified substantive corrective actions. | |||
01.2 Preoarations for Midlooo | |||
! | |||
a. Insoection Scooe (71707) | |||
l. Near the conclusion of its refueling outage. Unit 2 entered midloo) on | |||
! April 23 for vacuum refill of the Reactor Coolant System (RCS). Tie | |||
i inspector reviewed Generic Letter 88-17. Loss of Decay Heat Removal. | |||
! | |||
Catawba Nuclear Site Directive 3.1.30. Unit Shutdown Configuration | |||
Control. Rev. 8. and the operating 3rocedures governing the RCS | |||
, draindown to midloop, operation wit 1 reduced RCS inventory, and vacuum | |||
refill. The inspector conducted control room observations during the ! | |||
draindown to midloop and portions of unit operation at midloop. | |||
b. Observations and Findinos | |||
The inspector verified that the requirements delineated in Catawba l | |||
Nuclear Site Directive 3.1.30 were satisfied. Specifically, multiple : | |||
thermocouples were available for temperature monitoring; ultrasonics and | |||
sightglass indications were available for level monitoring: vital power | |||
was available from both offsite sources, as well as two emergency diesel | |||
generators; necessary emergency core cooling equipment was either | |||
operable or available: and the gravity flowpath criteria were satisfied | |||
for midloop operation with low decay heat. | |||
Just prior to reduced inventory operations, the inspector noticed that | |||
valves 2ND-33. Residual Heat Removal (RHR) System Return to the | |||
Refueling Water Storage Tank (FWST). 2FW-27A and 2FW-55B. RHR Pumps 2A | |||
and 2B Suction from the FWST. were available as opposed to operable. | |||
These valves are in the flowpaths of the three gravity feeds to the RCS. | |||
The valves were tagged closed in support of RCS maintenance. The | |||
, | |||
inspector questioned the a)proariateness of considering the associated | |||
! flowpaths available with tie RiR and FWST valves closed under a tagout. | |||
; | |||
! | |||
Enclosure 2 | |||
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l 4 | |||
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Normal makeup to the reactor coolant system via the chemical and volume | |||
control system was available. | |||
l The inspector inquired about the status of the RHR and FWST valves | |||
during reduced inventory and midloo) operations and determined that. | |||
, although they were tagged closed, t1e Work Control Center filed the tags | |||
l in a prominent location to facilitate equipment restoration in the event | |||
l that these valves were needed to mitigate a loss of RHR. | |||
: | |||
The inspector reviewed Catawba Nuclear Site Directive 3.1.30 to | |||
determine if administrative requirements were being met. The directive | |||
stated that, for midloop operations with low decay heat load, two ; | |||
l | |||
available gravity flowpaths were required. The directive defines i | |||
"available" as "the status of a system, structure or component that is ' | |||
in service or can be placed in service in a functional or operable state i | |||
by immediate manual or automatic actuation." The directive considers ! | |||
actions taken by operators to clear tags acceptable for restoring , | |||
equipment to functional or operable status within a reasonable period of l | |||
time. | |||
l | |||
The inspector raised a concern to the licensee that, while valves 2FW- | |||
27A. 2FW-55B. and 2ND-33 could possibly be restored to service in a | |||
. | |||
reasonable period of time, other components that might be impacted by | |||
the maintenance activity in progress might not be accounted for before ; | |||
the gravity flowpath would be utilized. Hence, points of compromised ' | |||
system integrity, which could allow flow to be diverted from the RCS. | |||
might be overlooked and either reduce the assumed flow to the RCS or ! | |||
extend the amount of time needed to place the gravity flowpath in | |||
service. Although no such conditions were identified during the midloop | |||
and vacuum refill evolutions, the licensee plans to evaluate Nuclear | |||
Site Directive 3.1.30 to determine if changes are warranted prior to the | |||
next refueling outage. | |||
c. Conclusions | |||
The inspector concluded that the draindown to midloop, midloop | |||
operation, and vacuum refill were conducted without incident. In | |||
general, the licensee implements effective controls for these | |||
. | |||
; | |||
evolutions. However, the inspector questioned the availability of 1 | |||
equipment required for gravity flow to the core and expressed concern | |||
that the process for restoring needed equipment may not be sufficiently | |||
controlled. | |||
01.3 Doerator Aid Comouter Installation and Comoensatory Action | |||
a. Insoection Scooe (71707) | |||
l During the Operator Aid Computer (OAC) installation, the inspector | |||
; periodically verified that the Loss of DAC procedure was implemented | |||
l while the OAC was unavailable. The inspector observed an open main | |||
Enclosure 2 | |||
( | |||
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' | |||
1 | |||
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5 , | |||
control room door and reviewed the associated compensatory action. | |||
" Control Room Pressure Boundary." dated March 20. 1997, to verify that | |||
the licensee had satisfied selected initial conditions that allowed the | |||
door to remain open. The inspector also evaluated the licensee's | |||
im)lementation of the compensatory action guidance following receipt of | |||
a Jnit 2 fuel handling building high radiation alarm that occurred on | |||
March 24. | |||
b. Observations and Findinas | |||
During the Unit 2 OAC installation. the OAC was not available for < | |||
l automatic surveillance of numerous plant parameters. As a result, the I | |||
control room operators were required to implement PT/1/A/4600/09. Loss | |||
of Operator Aid Computer, and perform those surveillances manually'on | |||
specified time intervals. The inspector periodically verified that the l | |||
procedure was in use while OAC monitoring was unavailable. Often a l | |||
dedicated reactor operator was available to perform this function. | |||
; | |||
' | |||
although that could not always be accommodated. The inspector | |||
determined that the procedure was in place and being implemented when | |||
required. | |||
l The inspector observed that the Unit 2 control room vital access door | |||
was opened on March 22 and was left open continuously to allow passage | |||
' | |||
. | |||
of a flexible ventilation duct (approx. 12 inch diameter). The duct was | |||
. | |||
I | |||
used to exhaust fumes generated from welding performed to install the | |||
replacement operator aid computer in the Unit 2 main control board | |||
panel. The inspector discussed the compensatory actions with | |||
engineering and operations 3ersonnel to determine if the compensatory | |||
actions would ensure that tie control room would pressurize sufficiently | |||
' | |||
to meet control room habitability requirements during design basis | |||
events. Both operations and engineering personnel stated the design | |||
basis for contrM room pressurization and habitability would be met | |||
provided that initic1 conditions of the compensatory action were | |||
satisfied and that the control room door would be manually closed, after | |||
separating a connection in the duct. if certain plant events (e.g.. | |||
safety injection signal) were to occur. | |||
The inspector verified that selected initial conditions were satisfied | |||
and found no discrepancies with the plant conditions that existed at the | |||
time of the inspection. The inspector observed, however, that the | |||
initial conditions of the compensatory action were not being | |||
periodically verified to ensure that plant changes since the initial | |||
condition verification on March 22 had not invalidated the assumptions | |||
supporting the compensatory action. Operations personnel informed the | |||
inspector that periodic verification of initial conditions for the | |||
compensatory actions was not required. | |||
l The inspector expressed a concern to the licensee that, because there | |||
l | |||
was a high number of initial conditions required for this particular | |||
compensatory action and because of the relatively long duration of the | |||
: | |||
Enclosure 2 | |||
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! 6 | |||
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replacement operator aid com) uter installation, periodic verification of | |||
initial conditions may have 3een warranted to ensure that necessary | |||
conditions continued to be met. Additionally, the licensee recognized | |||
that changes in plant ventilation equipment status created by refueling | |||
outage activities could invalidate the assumptions of the analysis | |||
supporting the compensatory action. | |||
l | |||
The licensee initiated timely corrective actions to periodically l | |||
reverify the initial conditions of the compensatory action. The i | |||
, | |||
periodicity of the reverification varied based on the potential for the ! | |||
l | |||
condition to change. The inspector observed the reverification of the - | |||
initial conditions following implementation of the licensee's corrective | |||
actions. | |||
l | |||
, | |||
The inspector observed two other minor discreaancies during the review | |||
of the compensatory action im)lementation. T1e control room door was | |||
i not closed on March 24 when tie Unit 2 spent fuel pool bridge radiation i | |||
monitor (2 EMF 4) alarmed although this appeared to be a condition for l | |||
; closing the door. The inspector determined that the radiological | |||
; conditions that caused the alarm were inconsequential and not related to ; | |||
l | |||
a release (refer to Section 01.5). The inspector also found that the | |||
accountability log sheet that specified individuals responsible for | |||
. | |||
manually closing the control room door had not been signed for one day. | |||
The inspector determined that the individuals involved were aware of | |||
l their responsibilities, but had committed an administrative error. < | |||
The licensee documented the inspector's concerns in Problem | |||
Investigation Process (PIP) Report 0-C97-0988 and initiated actions to | |||
l | |||
determine: (1) if the response to the alarm was appropriate: (2) the | |||
' | |||
cause of the administrative error: and (3) if a reverification process | |||
; for compensatory actions is needed. | |||
I c. Conclusions | |||
The inspector concluded that control room operators were appropriately | |||
l implementing their procedure for Loss of OAC when the OAC was | |||
unavailable during the installation process. Additionally, operator | |||
effectiveness in implementing a complex compensatory action was | |||
challenged by numerous initial conditions and the lack of periodic | |||
reverification to ensure that they were being continuously met. | |||
01.4 Boron Dilution Mitiaation System Reliability | |||
a. Insoection Scope (71707) | |||
Du' ring the Unit 2 shutdown for refueling outage 2E0C8. multiple problems | |||
, associated with the Boron Dilution Mitigation System (BDMS) were | |||
encountered. The inspector investigated the nature of each problem and | |||
reviewed the work history of the BDMS for both units. The inspector | |||
i | |||
Enclosure 2 | |||
l | |||
l | |||
l | |||
! | |||
- . . . - _ - . - . - - . .. . - - .. .. | |||
! | |||
. ! | |||
, | |||
7 l | |||
reviewed the FSAR and Technical Specifications (TS) and discussed system | |||
performance and vulnerabilities with engineering personnel. | |||
, | |||
b. Observations and Findinas | |||
The BDMS consists of two trains and is designed to protect the reactor . | |||
from an inadvertent criticality by automatically stopping the flow of i | |||
unborated water to the core during shutdown conditions. Required by TS | |||
in Modes 3, 4. 5. and 6. the BDMS uses two source range detectors to ' | |||
monitor the subcritical multiplication of the reactor core. An alarm , | |||
set)oint is continually calculated, and if the setpoint is exceeded, | |||
eitler train of BDMS will automatically shut off both reactor makeup | |||
water pumps, align the suction of the charging pumps to the Refueling | |||
Water Storage Tank (FWST), and isolate flow to the charging pumps from . | |||
the Volume Control Tank. Because these functions are automated, no | |||
operator action is required. | |||
Technical Specification 3.9.2 requires both trains of the BDMS to be | |||
operable during Mode 6. If one or bcth trains are inoperable, the | |||
licensee must either suspend core alterations or verify' that source + | |||
range neutron flux monitors are operable with alarm setpoints | |||
a)propriately calculated for the current (and, during core reload, | |||
clanging) steady-state count rate. The licensee also must take | |||
additional actions to verify that audible alarms are available in the | |||
control room and containment, and that reactor makeup water pump flow | |||
rates are within limits. In addition the BDMS is required operable | |||
during Modes 3, 4 and 5 by TF 3.3.3.11. | |||
kDuringtheUnit2refuelingoutage,multipleproblemswiththeBDMSwere | |||
encountered. On March 25. Unit 2 BDMS interlock testing revealed a | |||
failure to secure the reactor makeup water pumps. The failure was | |||
attributed to a failed optical isolator. On March 28 during core | |||
offload to the Spent Fuel Pool, a spike on the B train source range | |||
instrument caused the charging pump suction to swap from the Volume | |||
Control Tank to the FWST.' This spike was attributed to noise generated | |||
by welding activities during the Operator Aid Computer replacement and | |||
exacerbated by a loose plug at the data processing cabinet. A third | |||
problem, which also occurred during the core offload, was associated | |||
with a shutdown monitor that failed to a zero signal reading. Because | |||
of the latter two problems the BDMS was declared inoperable, and the | |||
required TS actions were performed. | |||
Problems with the BDMS had been encountered periodically in the past. | |||
According to the licensee's Work Management System (WMS), numerous work | |||
requests have been written since 1987 for the BDMS. Since 1986. 134 | |||
work requests have been closed for the Unit 1 BDMS: since 1987. 83 work | |||
requests have been closed for the Unit 2 BDMS. The inspector could not | |||
consistently determine if specific work requesis were generated to | |||
resolve system problems or if they were "onerated for other reasons | |||
(e.g. nameplate installation). Nonetheles:.. the volume of work requests | |||
Enclosure 2 | |||
, | |||
k | |||
b | |||
' | |||
t | |||
l | |||
.- ; | |||
' | |||
L ! | |||
l - | |||
, | |||
8 ! | |||
i | |||
related to this system seemed high. The inspector expressed to the t | |||
l licensee a concern with BDMS reliability and availability, as well as | |||
the resulting impact (i.e., additional calibrations and monitoring) to | |||
l control room operators. The licensee had come to the same conclusion * | |||
through a system review independent of the NRC's inspection. Based on ! | |||
their findings, the licensee had recently decided to incorporate the ! | |||
BDMS into the site's Top Equipment Problem Resolution (TEPR) program. l | |||
c. Conclusions | |||
t | |||
' | |||
Problems encountered with the BDMS during the' Unit 2 refueling outage | |||
. were indicative of historical system performance problems, which affect ; | |||
plant operation during modes 3. 4. 5 and 6. The inspector concluded I | |||
that, since additional monitoring and calibration activities are | |||
~ required when the BDMS is inoperable the BDMS has caused additional | |||
control room operator workload to compensate for its unreliability. The | |||
i- licensee has indicated that efforts are being initiated to improve | |||
system reliability and, thereby. reduce operator burden through the TEPR | |||
process. So that the licensee's efforts to correct this adverse system | |||
. | |||
' | |||
performance trend can be monitored to resolution, this issue is | |||
identified as Inspector Followup Item 50-413.414/97-07-02: Boron | |||
Dilution Mitigation System Reliability Resolution. | |||
:. | |||
01.5 Fuel Handlino Buildina Evacuation | |||
a. Insoection Scooe (71707) | |||
'The inspector evaluated the licensee's response to a radiation alarm | |||
resulting in an evacuation of the fuel handling building that occurred | |||
on March 24. The inspector reviewed licensee's procedures, conducted | |||
interviews with involved personnel, and walked down the fuel handling | |||
building. | |||
b. Observations and Findinas | |||
On March-24. the inspector responded to the control room when the , | |||
control room operators announced over the public address system the i | |||
evacuation of the fuel handling building. During this time, the water | |||
' | |||
level in the fuel transfer canal had been lowered to facilitate | |||
maintenance on valve 2KF-122. Fuel Transfer Canal Isolation Valve. The | |||
ins)ector found that the spent' fuel pool bridge radiation detector | |||
(2EiF-4) had alarmed, and annunciator response procedure for alarm 2- | |||
RAD-3 had been implemented. The control room o)erators conservatively | |||
elected.to evacuate the fuel handling building )ecause the ah:r.m was not ; | |||
expected.- The inspector verified that the control room operators i | |||
; properly followed their procedures and that the appropriate level of I | |||
supervisory oversight was maintained during the event. j | |||
' | |||
The inspector also discussed the event with Radiation Protection ' | |||
personnel and found that proper actions were completed. Radiation | |||
Enclosure 2 | |||
! | |||
I | |||
. - - | |||
- _ - . | |||
._ . _ _ _ _ _ _ _ . - _.._ _._. -e.__________...- _._ _ | |||
t | |||
; | |||
* | |||
i' . i | |||
. i | |||
! 9 { | |||
! | |||
! | |||
Protection technicians surveyed the area and reported back to the ; | |||
control room. Subsequently, the 2FME-4 alarm setpoint was raised to 2 | |||
three times the background radiation level in'accordance with approved ! | |||
procedures. Additionally, the inspector verified that the area survey : | |||
map for the fuel handling building was updated, and the associated i | |||
instrument log for 2 EMF-4 was changed to reflect-the new setpoint. ! | |||
l | |||
Because the alarm was not anticipated, the licensee initiated actions to i | |||
evaluate the root cause of the event and determine appropriate l' | |||
corrective action. Discussions with various plant )ersonnel revealed | |||
that better coordination between affected plant wort groups and a ! | |||
possible procedure enhancement were needed during fuel transfer canal i | |||
draining. This would provide for an increase in the alarm setpoint to i | |||
! | |||
accommodate the expected increase in background radiation levels in the i | |||
area with the canal drained. | |||
! On March 25. the inspector performed a walkdown of the fuel handling ! | |||
building for area familiarization. During the walkdown the inspector ' | |||
performed a housekeeping assessment with emphasis on the licensee's | |||
> | |||
adherence to foreign material exclusion (FME) requirements. ' The : | |||
l inspector found that miscellaneous items (e.g. safety belt, tool bag, 2 | |||
face shield. grease gun, and paper) i.ere on the transfer canal catwalk : | |||
. | |||
area and had not been logged into the cleanliness logbook. The licensee i | |||
subsequently issued PIP 2-C97-08/1 to document this NRC observation and | |||
i | |||
address corrective actions. ' | |||
i | |||
c. Conclusions | |||
. | |||
L | |||
The inspector concluded that actions by operations and RP personnel .in ' | |||
l response to the radiation alarm in the fuel handling building were good. " | |||
! However, administrative controls over FME were not pro)erly im)1emented | |||
t by personnel working near the fel transfer canal in t1e fuel landling | |||
building. | |||
01.6 Unit 1 Pressurizer Block Valve Control Circuit Failure | |||
a. Insaection Scone (71707. 61726. 62707) | |||
' | |||
On March 20, Unit 1 pressurizer Power 0)erated Relief Valve (PORV) block | |||
valve INC-33A failed.to. stroke closed w1en the valve control switch was | |||
placed in the closed position during surveillance testing. A similar | |||
failure of this valve had occurred on August 10, 1995. The inspector | |||
reviewed the licensee's immediate actions to comply with TS action | |||
requirements and an associated operability evaluation. The inspector | |||
also reviewed PIP documentation (1-C97-0781 and 1-C95-1204) and the | |||
licensee's evaluation of the potential repeat failure. | |||
' | |||
. | |||
: | |||
! | |||
:- Enclosure 2 | |||
. - . , -. . . | |||
- _ _ _ ._ __ | |||
* | |||
, | |||
I | |||
i | |||
10 | |||
b. Observations and Findinos | |||
The block valve is controlled with a three position control switch | |||
(open/close/ override). During the surveillance test the valve failed to | |||
close when the "close" Josition was selected. The licensee declared the - | |||
valve inoperable and suasequently succeeded in closing the valve using | |||
' | |||
the " override" position. The inspector verified that the licensee met . | |||
TS requirements after the valve was declared inoperable (TS 3.4.4. | |||
Relief Valves). | |||
Maintenance troubleshooting determined that the failure occurred in an | |||
interlock portion of the block valve's control circuit. The interlock ; | |||
uses position signals generated from stem mounted limit switches located , | |||
on the two other Unit 1 pressurizer PORV block valves. An operability l | |||
evaluation performed after troubleshooting efforts concluded that the ; | |||
block valve was operable since it would remain capable of closing as | |||
required using the " override" position. The licensee's investigation of l | |||
. | |||
the previous failure in 1995 found that a limit switch lever shaft had | |||
broken. The licensee has scheduled work orders to inspect the limit | |||
switches and block valves during the next refueling outage and will | |||
initiate further investigation if the same type of failure has occurred. J | |||
. c. Conclusions ' | |||
A Unit 1 pressurizer PORV block valve control circuit failure occurred | |||
which is a potential repeat of a previous 1995 failure. The licensee | |||
. | |||
I | |||
has planned appropriate actions to determine the cause of the control ' | |||
circuit component failure when the components are accessible at the next | |||
refueling outage. | |||
08 Miscellaneous Operations Issues (92901. 92902) | |||
08.1 (Closed) VIO 50-413.414/94-13-01: Failure To Follow Procedure NSD 703 4 | |||
And Station Directive 34.0.5 Requirements. | |||
The inspectors reviewed the corrective actions identified by the | |||
licensee for this violation in letters dated August 15. 1994, and August | |||
8.1995, and verified that these actions were reasonable and complete. | |||
The licensee's evaluation substantiated the violation and identified ' | |||
approximately 600 comaonents which were provided with an identification ' | |||
tag that identified t1e component number, but the tag did not include | |||
the component's noun name as required by the site's procedures. The | |||
inspectors performed a sample inspection of these components and ! | |||
verified that the identification tag included both the component number | |||
and noun name. 4 | |||
l | |||
l | |||
! | |||
Enclosure 2 | |||
l | |||
l | |||
! | |||
l | |||
- __ _ _ _ _ ._ __ _ _ _ _ _ _ _ _ _ _ _ __ | |||
, | |||
* | |||
. | |||
. | |||
11 | |||
08.2 (Closed) VIO 50-413/95-07-01: Inadequate Modification Procedure | |||
Resulting in Loss of RHR. | |||
TN/1/A/1331/00/01A. Procedure for the Implementation of NSM CN-11331. | |||
Work Unit 01. did not receive adequate cross disciplinary review to | |||
determine operational impact and scheduling to determine a safe plant | |||
condition for implementation. The licensee's response dated April 28, | |||
1995. stated that immediate actions were taken to revise the procedure | |||
and stop work on modification implementation until all modification | |||
packages were reviewed for similar errors. Additionally, the licensee | |||
formed two self-assessment teams to determine root cause of the event. | |||
The modification process was also revised to add new screening criteria I | |||
for critical modifications that require an independent Senior Reactor 1 | |||
0)erator review to determine safe plant conditions for implementation of i | |||
t1ese modifications. The inspector reviewed corrective action j | |||
documentation (PIP 1-C95-0203) and verified that the licensee completed | |||
these actions. | |||
08.3 (Closed) VIO 50-413.414/95-07-02: Inadequate Valve Verification | |||
Activities - Two Examples. | |||
l | |||
l Both examples of the violation involved personnel that failed to use | |||
. | |||
proper verification methods or independent verification of determining l | |||
l | |||
valve position or valve location. The licensee's response dated April l | |||
! 28, 1995, stated that procedure revisions and additional training was l | |||
provided for the plant staff that is involved in these verification | |||
activities. The ins)ector verified that Operations Management Procedure | |||
2-33. Valve and Breacer Position Verification and Valve Operations, was | |||
revised to provide guidance for verifying the position of deenergized | |||
motor operated valves. In addition, the licensee provided training to | |||
, establish worker skills in error reduction. The inspector concluded | |||
that the licensee's corrective actions were appropriate. j | |||
1 | |||
l II. Mainwunce | |||
M1 Conduct of Maintenance | |||
1 | |||
1 | |||
M1.1 Unit 2 Outaae Maintenance Items | |||
a. Insoection Scope (62707) | |||
l The resident inspector monitored and inspected various work items during l | |||
l the Unit 2 E0C8 refueling outage. Among these were: (1) a modification : | |||
to replace the 2A and 2B Emergency Diesel Generator (DG) battery | |||
chargers: (2) inspection and preventive maintenance on the 2B DG: (3) | |||
the inspection and reconditioning of valves in the Safety Injection (NI) | |||
system: (4) the repair of Loose Parts Monitoring System Channel 17. | |||
Steam Generator (SG) manway: (5) the inspection of the containment sump | |||
recirculation valve 2NI-185B: and (6) inspection of the A and D Reactor | |||
! Coolant Pump (RCP) number 1 seals. The inspector discussed the | |||
Enclosure 2 | |||
i | |||
! | |||
l | |||
._ . . .. _ _ _ _ - _ . . _ _ . _ . _ . _ _ _ ___. _ . .. _ | |||
' | |||
. | |||
. | |||
12 | |||
maintenance activities with the licensee, obtained copies of the work | |||
packages and observed portions of the maintenance in progress. | |||
b, Observations and Findings | |||
l' | |||
(1) The Unit 2 125 Volt DC DG battery chargers were replaced under | |||
station modification CN-21360. The inspector reviewed the work | |||
Jackages associated with TN/2/A/1360/00/02E, which governed the A | |||
Xi battery charger replacement., and TN/2/A/1360/00/03E, which | |||
governed the B DG battery charger replacement. The inspector | |||
verified that an 8-hour load test on DG chargers- 2A and 28 a | |||
polarity check, output voltage check and current check were , | |||
successfully completed before the battery chargers were installed. | |||
Steel frames and grout pads were fabricated for the chargers. The | |||
inspector also verified that provisions for maintaining electrical i | |||
separation, fabricating and installing electrical enclosures, | |||
grounding cables, sealing the cable terminations, and using | |||
crimping tools were included in the work packages. Cable | |||
installation was ')rocedurally controlled, and electrical | |||
isolations and ca]le terminations were recorded in the associated | |||
procedure. A charger capacity test was satisfactorily performed, | |||
the battery was equalized and charged, batteries were inspected. | |||
. and the charger's high and low voltage relay alarms were | |||
calibrated. | |||
(2) The inspection and maintenance plan for the 2B DG included | |||
activities typically performed on a five-year interval. The | |||
l inspector observed portions of the activities in progress and | |||
reviewed the work package and associated work orders, The | |||
licensee disassembled sections of the DG: cleaned the engine | |||
block; replaced hoses: refurbished the engine-driven fuel oil | |||
pump: inspected cams and rollers: inspected the jacket cooling | |||
water pump drive gear: inspected strainers for the starting air | |||
system; and inspected and refurbished a temperature regulating | |||
valve in the DG jacket cooling water system. | |||
(3) Multiple check valves, suspected of leaking, were inspected during | |||
l the outage. The licensee inspected valve 2NI-171, Safety | |||
, Injection pumps to RCS loop C cold leg injection header check | |||
valve, and determined that the valve had low seating contact. A | |||
l minor modification was generated, and the disc was replaced with a | |||
new disc of a different design that provided better seating | |||
integrity. | |||
Valve 2NI-175. RHR header A to RCS Loop C cold leg check valve, | |||
was inspected: the valve was cycled, and the disc operated freely , | |||
without binding. The valve body and disc seats had no indication H | |||
of degradation. The valve body and disc seats were cleaned, and a ' | |||
visual inspection revealed wide seat contact. | |||
, Enclosure 2 | |||
i | |||
; | |||
: | |||
l l | |||
_ .._ _ . - . _ _ _ . . ._ _ _ _.._ _ _ _ _ _ __.__ _ | |||
: | |||
' | |||
' | |||
l . | |||
~ | |||
, | |||
13 | |||
' | |||
Valve 2NI-176 RHR Header A to RCS Looi D cold leg check valve. | |||
showed no evidence of seat wear or leacage. The licensee cleaned | |||
the seating surfaces and determined that they were finely. polished | |||
. | |||
' | |||
with no indication of degradation. | |||
l The disc in valve 2N!.-169. Safety Injection pumps to RCS lcop D | |||
l cold leg injection header, was replaced, and the valve body seat | |||
l was lapped until good contact could be visually verified. A-small | |||
! | |||
defect was polished out of the valve bonnet. The defect was i | |||
believed to have caused minor external leakage in December 1995 | |||
and had been seal welded at that time to stop the leakage. | |||
The inspector did not identify any concerns associated with the NI | |||
system check valve maintenance. | |||
(4) Unit 2 Loose Parts Monitoring System Channel 17. SG manway, was | |||
repaired during a forced outage in December 1996. The channel had | |||
been declared inoperable on January 2, 1996. Subsequent | |||
troubleshooting revealed that the failure of the channel | |||
, | |||
' originated in the field. The licensee initiated a work request to | |||
repair the channel during an outage window, at which time the | |||
necessary containment entry could be made. To notify the NRC that | |||
. | |||
Channel 17 of the Loose Parts Monitoring System was inoperable for | |||
. | |||
longer that 30 days, the licensee submitted a s)ecial report on | |||
l February 11, 1996, in accordance with Selected .icensee | |||
Commitment Section 16.7-4, and TS 6.9.2. | |||
The inspector discussed the repair with licensee personnel, | |||
reviewed the associated work order. WO 96000758-01, and verified , | |||
that the channel )roblem had been corrected. The licensee had | |||
determined that tie acoustic sensor' had an open _ connector at the- : | |||
: | |||
female hard line connector point. The sensor was replaced and- | |||
! | |||
satisfactorily tested. The channel was returned to service on | |||
December 16, 1997. | |||
(5) Prior to the last refueling outage-(2EOC7) the licensee determined | |||
! that containment sump recirculation valves NI-184A and NI-185B. | |||
l double-disc gate valves, were susceptible to pressure locking. | |||
! During 2EOC7 the licensee im)lemented a station modification to | |||
l , | |||
install a bonnet vent on eac1 sump recirculation valve. The > | |||
1 | |||
bonnet vents provided a relief path from the valve body to the | |||
residual heat removal (RHR) aump discharge line to preclude | |||
pressurization in the valve Jody and subsequent wedging of the | |||
i | |||
' | |||
valve discs into their respective seats. The bonnet vent valves | |||
were intended to remain open during full )ower o)erations, | |||
although they could be. closed to isolate RHR leacage past the | |||
7 containment-side valve disc. | |||
I During startup from the- previous refueling outage. 2EOC7.- the | |||
i | |||
licensee determined that the containment-side seat of 2NI-185A was | |||
; | |||
. | |||
Enclosure 2 | |||
l | |||
\ | |||
. | |||
i . -. - - | |||
. | |||
. . _. _ ._._. .. _ _ _ . _ . . _ _ _ _ . . . . _ _ _ _ _ _ _ . _ _ | |||
, | |||
- | |||
I | |||
. | |||
i | |||
. | |||
l 14 i | |||
> | |||
leaking. Since the bonnet vent valve (2NI-488) bypassed the RHR : | |||
i suction-side disc a minor flow 3ath was created from the FWST. ! | |||
L via the RHR suction header. to t1e containment sump. To block the ! | |||
l leakage, vent valve 2NI-488 was locked closed. A work order was i | |||
; generated to inspect and repair 2NI-185B during 2E0C8. ; | |||
l The licensee opened the valve to inspect the seatirig surfaces l | |||
during the refueling outage: the inspection results were | |||
~ | |||
l | |||
documented in PIP 2-C97-1066. At several locations around the ' | |||
perimeter of the containment-side valve body seat, small | |||
l semicircular indicat ions were visible. The containment-side disc | |||
l- seat had similar marks where the two surfaces had mated. The i | |||
licensee could not determine why the pattern was present on the ' | |||
l valve body seat, nor coula the valve vendor explain these ! | |||
; indications. The indications in the seat surfaces were the likely ! | |||
! cause of the seat leakage during the previous operating cycle. | |||
) | |||
l | |||
' | |||
The licensee opted to leave the valve in its as found condition to ! | |||
avoid disturbing the seating of the RHR-side disc. The inspector i | |||
, | |||
' | |||
questioned this decision, since they had been aware of the seat : | |||
leakage during the preceding operating cycle and had ample time to , | |||
l plan for re) air during the refueling outage. The licensee ! | |||
l. explained tlat extensive time and resources could be allocated to i | |||
l improve the containment-side di.;c seating, but that improvement | |||
j. could not be guaranteed and that the RHR-side disc seating ' | |||
; integrity could be disturbed in the process. i | |||
To test valve seating integrity.of the containment-side disc. the < | |||
licensee applied 50 psig from the RHR pump side of the valve with | |||
l vent valve 2NI-488 closed: no signs of leakage into the , | |||
' | |||
containment sump were identified. Valve 2NI-488 was then' opened. ! | |||
! and leakage into the sump was observed. Valve DI-488 was then | |||
: closed, and leakage into the sump was isolated oy the seating | |||
l integrity of the RHR-side disc and the bonnet vent valve. An i | |||
operability evaluation, documented in PIP 2-C97-1172. stated that | |||
(1) valve 2NI-488 will be administratively controlled in the- l | |||
closed position, and (2) valve 2NI-185A is operable with 2NI-488 | |||
, closed. The inspector concluded that the o)erability evaluation | |||
i and actions taken to address seat leakage w1ile accounting for | |||
! pressure locking and thermal binding were appropriate. | |||
(6) The inspector observed RCP seal inspections and maintenance. The | |||
! ins)ector also reviewed the task completian comments associated | |||
wit 1 work orders 96098973-01 and 96098974-01 (for 2A and 2D RCP | |||
seal work, respectively). The 2D RCP numoer 1 seal was cleaned | |||
and inspected verified to be in good condition. and reinstalled. | |||
, A chip was found in the outer edge of the 2A 'RCP number 1 seal | |||
' | |||
surface. A new set of stationary and running seals was installed, | |||
j and the maintenance personnel verified that the seal moved freely | |||
j up and down. | |||
' | |||
Enclosure 2 | |||
i | |||
i | |||
i | |||
! | |||
! | |||
l | |||
l .. . - - | |||
. . . .- --- - - .. . . - . . | |||
* | |||
. | |||
i | |||
. | |||
15 | |||
The inspector noted that RCP seal work was conducted in confined | |||
areas around the RCPs. The work areas were difficult to access | |||
and cramped. In addition, cleanliness and lighting levels during | |||
the maintenance activities were adversely affected by the cramped | |||
working spaces. | |||
c. Conclusions | |||
The inspector concluded that, in general, outage-related maintenance ' | |||
activities were ap]ropriately conducted. Although multiple barriers to | |||
minimizing the risc of human error during RCP seal maintenance were | |||
noted, the ins)ector was unaware of any human performance problems | |||
associated wit 1 the work. | |||
M1.2 Unit 2 Nuclear Service Water Pumo Motor Reolacement | |||
a. Insoection Scope (62707) | |||
The inspector reviewed the licensee's resolution to elevated vibration | |||
levels associated with the 2B nuclear service water pump / motor assembly. | |||
The 2B nuclear service water pump has experienced intermittent periods | |||
of elevated vibration since 1994. During the inspection period, the | |||
. licensee identified problems with the condition of the s | |||
service water replacement motor stored in the warehouse.Accordingly, | |||
pare nuclear | |||
the inspector reviewed the results of previous licensee assessments of | |||
spare motor storage practices, previous motor failures, and an ongoing | |||
licensee assessment of maintenance and storage practices for spare | |||
motors. | |||
b. Observations and Findinas | |||
The 28 Nuclear Service Water pump is a smooth running pump with normally | |||
low measured vibration levels. In 1994 and 1995 the pump / motor assembly | |||
3eriodically experienced an increase in vibration relative to its past | |||
)aseline performance and also relative to the other nuclear service | |||
water pumps. The relative increase in vibration levels caused the pump | |||
to enter Alert levels although it continued to remain in the smooth | |||
running range, As a result of this experience, the licensee performed | |||
extensive inspection of this pump and motor during the current refueling | |||
outage. Internal inspection of the pump showed no damage or | |||
degradation. Vibration measurements made during an uncoupled run of the | |||
motor indicated that the source of elevated vibrations was confined to | |||
the motor. Based on additional analysis of vibration dr.ta performed by ' | |||
Electrical System Support (ESS) personnel, the licensee determined that | |||
an internal rub was occurring in the motor and elected to replace it. | |||
The spare nuclear service water pump motor developed severe oil leaks | |||
' | |||
from its lower bearing during initial check out runs performed in the | |||
motor test shop prior to its installation. Inspections of the saare | |||
motor internals performed by an offsite vendor determined that tie lower | |||
Enclosure 2 | |||
: | |||
I | |||
. __ , -. -. | |||
* | |||
. | |||
_ | |||
16 | |||
bearing surfaces were partially melted due to rubbing or inadequate | |||
lubrication. Additional testing revealed more problems and the spare | |||
motor was considered unacceptable for use and required extensive rework | |||
and repair. The licensee subsequently performed internal inspections of l | |||
the installed nuclear service water pump motor and determined the cause I | |||
of the eleyated vibration resulted from mechanical looseness in the , | |||
upper bearing components. An off center condition in the lower bearing 1 | |||
housing was also discovered. The licensee corrected these ' | |||
adeficiencies, which eliminated the elevated vibration characteristic as i | |||
measured in uncoupled runs and coupled inservice pump tests. l | |||
In 1996, a residual heat removal pump motor failed soon after functional | |||
testing. The licensee determined that poor storage conditions may have | |||
contributed to this failure (refer to NRC Inspection Report 96-13). The | |||
licensee has recently performed two assessments of motor storage and I | |||
handling practices and identified several findings and recommendations. I | |||
Inspector Followup Item (IFI) 50-413.414/97-07-03, Review Corrective | |||
Actions For Storage and Handling Assessment Findings, is identified to | |||
verify that the licensee has completed corrective actions resulting from | |||
the followirig assessments: (1) Assessment Report CTS-09-96. Electric i | |||
Motor P.M. - 12/2/96; and (2) Assessment Report SA-97-61(CN)(SRG), j | |||
Assessment of Warehouse Material Condition - 4/23-28/97. | |||
. | |||
c. Conclusions | |||
The licensee's resolution of long-standing elevated vibration levels , | |||
associated with the Unit 2B nuclear service water pump motor was very ! | |||
good. Deficiencies identified with a spare nuclear service water pump | |||
motor, a previous motor failure, and findings identified by licensee | |||
assessment of warehouse storage and handling 3ractices raised questions | |||
about control and storage of spare motors. T1e issue is identified as | |||
an Inspector Followup Item and will be reviewed during a future | |||
inspection. | |||
1 | |||
M2 Maintenance and Material Condition of Facilities and Equipment | |||
M2.1 Observation of Unit 2 Inservice Insoection Work Activities | |||
a. Insoection Scope (73753) | |||
The present Unit 2 E0C8 refueling outage was the first outage, of the | |||
first inspection period, of the second inservice inspection interval. | |||
The applicable code for Unit 2, for the second inservice inspection | |||
interval was the American Society of Mechanical Engineers (ASME) Code | |||
l Section XI, 1989 Edition, no Addenda. The inspector reviewed | |||
l documentation and observed ultrasonic, magnetic ) article, and liquid | |||
l | |||
~ | |||
penetrant examination activities to determined w1 ether the inservice | |||
inspection (ISI) activities were performed in accordance with Technical | |||
specifications (TS), the applicable ASME Code, and/or requirements | |||
imposed by NRC/ industry initiatives. | |||
' | |||
Enclosure 2 | |||
l | |||
1 | |||
* | |||
. | |||
17 | |||
b. Observations and Findinos | |||
The inspector reviewed the ISI outage examination plan and certification | |||
records for all NDE examiners aerforming ISI examinations this outage. | |||
l The following procedures, whic1 were used in the examination activities | |||
observed by the inspector, were reviewed for technical content: | |||
* NDE-600. " Ultrasonic Examination of Similar Metal Welds in Wrought l | |||
Ferritic and Austenitic Piping." Revision 9 | |||
. | |||
NDE-610. " Ultrasonic Examination of Dissimilar Metal Welds and | |||
Cast Austenitic Welds Using Refracted Longitudinal and Shear i | |||
Waves." Revision 4 | |||
. | |||
NDE-660 " Ultrasonic Examination of Reactor Pressure Vessel Head | |||
to Flange Welds." Revision 2 | |||
. NDE-25. " Magnetic Particle Examination." Revision 17 | |||
. NDE-35. " Liquid Penetrant Examination." Revision 16 | |||
Examinations of the following components were also observed by the | |||
. inspector to determine if the examination procedures were followed, | |||
whether examination personnel were knowledgeable of the examination | |||
method and operation of the test equipment, and if the examination | |||
results and evaluation of the results were recorded as specified in the | |||
ISI program and NDE procedures. | |||
. Welds Examined NDE Method Used | |||
2RPV-101-101*** Ultrasonic Examination | |||
2RPV-102-101*** Ultrasonic Examination | |||
2CA-59-8 Ultrasonic Examination | |||
2CA-59-11 Ultrasonic Examination | |||
2RPV-101-101 Magnetic Particle Examination i | |||
2CA-59-8 Magnetic Particle Examination i | |||
2CA-59-11 Magnetic Particle Examination | |||
2NV-242-3 Liquid Penetrant Examination | |||
2NV-242-4 Liquid Penetrant Examination | |||
2NV-242-10 Liquid Penetrant Examination 1 | |||
2NV-242-11 Liquid Penetrant Examination l | |||
2RPV-W80-101SE Liquid Penetrant Examination i | |||
2RPV-W81-101SE Liquid Penetrant Examination | |||
2RPV-W82-101SE Liquid Penetrant Examination | |||
2RPV-W79-101SE Liquid Penetrant Examination | |||
2RPV-W80-101 Liquid Penetrant Examination | |||
, 2RPV-W81-101 Liquid Penetrant Examination | |||
l 2RPV-W82-101 Liquid Penetrant Examination | |||
l 2RPV-W79-101 Liquid Penetrant Examination | |||
! | |||
! Enclosure 2 | |||
_ _ . __ _ _-. _ _ .. . _ . . | |||
. | |||
, | |||
, | |||
, | |||
. | |||
18 | |||
**** Note: Only portions of the 0 degree and 45 degree scans for these ! | |||
, | |||
reactor vessel head welds were observed due to radiation dose > | |||
limitations. | |||
' | |||
I | |||
l | |||
c. Conclusion | |||
NDE personnel certifications records, weld examinations, and NDE | |||
examination procedures were in accordance with Code requirements. | |||
M2.2 Observation of Unit 2 Steam Generator Eddy Current Data Acouisition | |||
Activities | |||
a. Insoection Scooe (73753) | |||
The inspector reviewed documentation and observed eddy current data , | |||
l acquisition activities to dstermine whether these activities were i | |||
performed in accordance with Technical Specifications (TS), the 1989 j | |||
Edition of Section XI to the ASME Code, and requirements imposed by - | |||
NRC/ industry initiatives. , | |||
; | |||
; | |||
b. Observations and Findinas | |||
, | |||
i | |||
l. The licensee was performing bobbin coil eddy current examinations of 62% ! | |||
of the tubes in all four steam generators for Unit 2. In addition, a i | |||
25% sample of the hot leg tube sheet transitions in each steam generator ' | |||
will be examined using a motor rotating pancake coil (MRPC). At the | |||
time of this ins)ection the licensee had just started the examination | |||
; activities and t1e data acquired was being sent directly to the McGuire | |||
' | |||
Nuclear Plant for analysis. Therefore, the inspector's examination of | |||
l | |||
' | |||
these activities was limited to review of the outage eddy current | |||
inspection plan, examiner and equipment certifications, and review of | |||
l | |||
examination procedures No. NDE-707 Revision 3, "Multifrequency Eddy | |||
Current Examination of Non-Ferrous Tubing. Sleeves and Plugs Using a | |||
Motorized Rotating Coil Probe", and No. NDE-701 Revision 3. | |||
"Multifrequency Eddy Current Examination of Steam Generator Tubing at | |||
McGuire. Catawba and Oconee Nuclear Stations and observation of the eddy | |||
. | |||
i | |||
current data acquisition process, | |||
l- c. Conclusion | |||
Review of the eddy current outage plan, equipment setup and acquisition | |||
procedures, personnel and equipment certifications, and observation of | |||
l data acquisition activities revealed that required documentation was | |||
l available and complete. and data acquisition personnel were | |||
l knowledgeable of the eddy current examination process. | |||
l | |||
! | |||
4 | |||
U | |||
. | |||
Enclosure 2 | |||
i | |||
l | |||
l | |||
' | |||
e | |||
19 | |||
M2.3 Unit 2 Flow Accelerated Corrosion (FAC) Proaram l | |||
a. Insoection Scooe (49001) ! | |||
l | |||
The inspector held discussions with the licensee's erosion / corrosion ! | |||
engineers to determine the scope of FAC examinations scheduled for this | |||
outage: the condition of the plant piping as revealed by inspection: the | |||
extent of pipe replacement recuired: and whether proper examination | |||
expansion was performed when cefective components were found. | |||
b. Observations and Findinas | |||
i | |||
The licensee's FAC program for Unit 2 was based on the Electric Power | |||
Research Institute's (EPRI) Document No. NSAC-202L. " Recommendation for | |||
an Effective Flow Accelerated Corrosion Program." Revision 1. In , | |||
addition. EPRI's CHEC Works Computer Codes were used, as well as ' | |||
portions of the licensee's prev'ous program for erosion / corrosion to | |||
identify components which will require examination. Initially, a sample | |||
of 55 components were scheduled for ultrasonic examination during the | |||
EOC-8 refueling outage. The sample also included the entire component. | |||
upstream and downstream of the initial component. The licensee planned ! | |||
to replace six components without further examination, based on ' | |||
. | |||
corrosion growth rates confirmed last outage. The examination of | |||
components for FAC this outage were approximately 40% complete when | |||
audited by the inspector. As a result of these examinations, five | |||
additional components will be replaced this outage. The inspector | |||
verified that expansion ins)ections.were correctly performed as a result | |||
of the components found to 3e unacceptable based on inspections | |||
performed this outage. The inspector also inquired as to why the | |||
initial inspection sample was so small. The licensee stated that | |||
smaller samples with a high volume of essential components. based on | |||
tracking and trending was now possible on Unit 2 for the following | |||
reasons: | |||
. Significant previous replacements of components with | |||
erosion / corrosion resistant materials. | |||
. Changes in secondary chemistry control have reduced wear rates | |||
significantly. | |||
. The entire upstream and downstream components from a sample | |||
' | |||
selected for inspection are also examined. | |||
. Unit 2 was designed with heater drains and moisturizer separator | |||
reheater drains which have erosion / corrosion resistant materials | |||
downstream of all control valves. | |||
. FAC program maturity. | |||
The inspector agreed with the licensee's reasoning. | |||
, Enclosure 2 | |||
: | |||
! | |||
l | |||
. . - . _ . _ | |||
l | |||
l | |||
. | |||
. | |||
20 I | |||
i | |||
c. Conclusion | |||
, | |||
The licensee has implemented an effective program for the detection of ) | |||
l | |||
' | |||
flow accelerated corrosion in components. This program was based on ' | |||
recommendations found in recognized industry standards. ! | |||
M7 Quality Assurance In Maintenance Activities . | |||
l M7.1 Maintenance Self Assessment Prooram | |||
a. Insoection Scone (62707. 40500) | |||
The inspector reviewed the status of maintenance and work control self- | |||
assessment programs. The inspection included review of NSD 607. Self- | |||
Assessments; maintenance and work control annual assessment plans for i | |||
1996 and 1997: selected self-assessment reports; and maintenance / work l | |||
control performance indicators, | |||
b Observations and Findinas | |||
The licensee's self-assessment program consisted of two types of self- l | |||
assessments, routine and non-routine. Routine assessments were | |||
'. performed on a quarterly or semi-annual basis and included topics such j | |||
as PIPS, Job Observations. Rework. Material Condition / Housekeeping. Work | |||
Order Quality. Budget. Radiation Dose / Contamination. Planning, and Work | |||
Control Process. Non-routine assessments were performed when the need i | |||
was apparent to management to assess a certain area or function. Some 1 | |||
examples were Procedure Use and Adherence. Environmental Compliance. | |||
Pre-job Briefings. Control of Vendors, and Work Task Skills. Corrective | |||
actions from the self-assessments were tracked for completion through | |||
PIPS. | |||
The inspector noted that the self-assessments that were reviewed ! | |||
effectively identified areas for improvement, and appropriate corrective ' | |||
actions were recommended and entered in the Problem Investigation ' | |||
Process for resolution. Of the routine assessments reviewed the | |||
inspector considered the quarterly assessment of Job Observation Trends, | |||
initiated in 1997, to be an effective use of the data generated by first | |||
line supervisor observations. | |||
Since the initiation of the Maintenance / Work Control Self-Assessment | |||
Programs in mid and late 1995. performance indicators such as work order | |||
backlog, schedule efficiency, and control board indication problems all | |||
showed improving trends. | |||
c. Conclusion ; | |||
' | |||
Based on the inspection described above. the inspector concluded that | |||
the maintenance / work control self-assessment programs effectively | |||
i | |||
identified areas for improvement and appropriate corrective actions. | |||
Enclosure 2 4 | |||
' | |||
l | |||
. - - . __ _... . _ . _ . . . . _ _ . _ . _ _ . . _ _ _ . _ . - . . _ . _ _ _ . _ . . _ . _ | |||
c' l | |||
* | |||
l . | |||
. | |||
21 , | |||
1 | |||
The self-assessments apparently contributed to improvemert. in the | |||
performance of the Maintenance and Work Control organizations. | |||
III. Enaineering | |||
I | |||
' | |||
El Conduct of Engineering | |||
El.1 Unit 2 Control Rod Tio Crackina | |||
l | |||
; | |||
a. Insoection Scoce (61726. 37551) | |||
During routine outage related examinations of Unit 2 control rod . | |||
, | |||
assemblies, the licensee identified a higher than expected number of | |||
! control rods with tip cracking. The inspector reviewed the licensee's | |||
L testing procedure, results of the examinations, and corrective actions | |||
;_ for test failures, | |||
b. Observations and Findinos | |||
l Industry experience has shown that control rods develop tip cracking as | |||
! a result of cladding interaction caused by swelling of the absorber | |||
l | |||
material inside this portion of the rods. . Tip cracking and other | |||
. | |||
potential control rod defects such as mechanical wearing are monitored | |||
every refueling outage by the licensee using procedure PT/0/A/4150/26. | |||
Rod Control Cluster Assembly (RCCA) Ultrasonic / Eddy Current Testing. , | |||
The inspector. discussed the results of the testing with reactor ' | |||
engineering personnel. The inspector observed that twenty.six control | |||
rod assemblies were found with indications of tip cracking. This | |||
- | |||
exceeded the expected number of twelve control rod assemblies aredicted , | |||
to have tip cracks The licensee ordered additional rod assem) lies ' | |||
fabricated by the vendor and replaced each control rod assembly that had- | |||
evidence of tip cracking. The inspector verified by reviewing control | |||
rod assembly deficiency evaluations that the twenty six assemblies were | |||
replaced. ' | |||
c. Conclusions | |||
The licensee's actions to replace all control rod assemblies that had | |||
evidence of tip cracking were appropriate. | |||
E2 Engineering Support of Facilities and Equipment | |||
E2.1 Review of Tentative Repair Activities for the Manway Cover on the Unit 2 | |||
Pressurizer | |||
a. Insoection Scone (62001) | |||
! | |||
l The Catawba Unit 2 pressurizer manway cover experienced a leak during | |||
i the end of cycle 8 shutdown for refueling. To repair the leak, the | |||
; licensee elected to use an alternate method of repair consisting of a | |||
1 | |||
; Enclosure 2 | |||
: | |||
i | |||
i | |||
, | |||
,_ , w g. . - - - - | |||
-. .- . - | |||
l | |||
' | |||
. | |||
. | |||
, 22 | |||
l | |||
welded diaphragm, in lieu of a flexitallic gasket. The licensee also | |||
planned to replace the bolts and nuts on the manway cover with studs and | |||
nuts. Another issue addressed in this modification was the inspection | |||
; and clean-up of the boric acid which had leaked from the flange of the | |||
! | |||
manway behind the insulation on the pressurizer. The inspector | |||
; reviewed this modification to ensure that documentation required for | |||
! | |||
this repair was available, and that inspection and cleanup of the boric , | |||
l acid crystals behind the pressurizer was properly addressed. 1 | |||
b. Observations and Findinas | |||
' | |||
In 1987, the licensee experienced several stuck bolts on the Unit 1 | |||
pressurizer manway. At that time the licensee used the alternate method | |||
of repair delineated in the Westinghouse Technical Manual for the | |||
pressurizer. This repair consisted of using a welded diaphragm, in lieu | |||
of a flexitallic gasket. In addition, the licensee substituted studs | |||
for the bolts used in the manway flange. At that time the licensee also | |||
l realized that this same modification may some day be required for Unit | |||
2. so 10 CFR 50.59 evaluations for the alternate modification method and | |||
calculations for the stress analysis of the studs and nuts were ! | |||
conducted for each Unit in 1987. The inspector reviewed this I | |||
documentation as well as the Westinghouse Pressurizer Technical Manual | |||
. and drawings for this alternate method of repair. The information | |||
reviewed was found to be satisfactory. | |||
, | |||
The inspector was initially concerned with the licensee's tentative I | |||
plans to remove insulation only from the top and bottom of the | |||
pressurizer in order to flush the boric acid crystals from behind the | |||
insulation, and to use technical justification based on boric acid | |||
corrosion rates documented in an EPRI document (TR-102748S) for | |||
acceptance of any possible damage to the pressurizer. The inspector's | |||
concern was based on the fact that the corrosion rates given in the EPRI | |||
document differed significantly from the corrosion rates established by | |||
Westinghouse under similar conditions and documented in NRC Generic | |||
Letter 88-05 " Boric Acid Corrosion of Carbon Steel Reactor Pressure | |||
Boundary Components in Pressurized Water Reactor Plants". In addition, | |||
the inspector did not believe that the plan to use technical | |||
justification met the intent of Catawba's Nuclear Site Directive 3.3.16. | |||
which stated. "When there is evidence that boric acid has run under ! | |||
insulation remove enough insulation during the inspection 3rocess to l | |||
assure all boric acid has been identified and evaluated. S1ould the | |||
investigation reveal no damage to the contaminated components, the area l | |||
is to be cleaned until free of visible borori crystals." During | |||
discussions held with senior licensee management, the inspector was | |||
informed that the plans for boric acid damage examination and flushing | |||
, on the pressurizer which were identified to the inspector were very | |||
' tentative and only one of many options being considered. The inspector ' | |||
l was also informed that a meeting on this issue was planned for following | |||
i | |||
week and the decisions reached in this meeting would be forwarded to the ) | |||
i inspector for review. l | |||
Enclosure 2 | |||
I: | |||
. . - - - - | |||
- | |||
, | |||
, | |||
. | |||
23 | |||
On April 9.1997, the inspector was informed of the licensee plans for | |||
inspection and cleaning of boric acid on the pressurizer. These plans | |||
would remove three additional sections of insulation and would allow | |||
visual inspection to be performed in spot locations from the top to the | |||
bottom of the pressurizer. The only disadvantage was visual inspection | |||
could only be performed on the lower side of each of the sup) ort rings | |||
except the top support ring. The licensee proposed that teclnical | |||
l justification be used for the acceptance of the up)er portion of each | |||
support ring using the EPRI criteria which Westinglouse agreed was | |||
, | |||
a)propriate for this corrosion wear application. These actions resolved | |||
! | |||
t1e inspector's concerns. | |||
l The licensee )lanned to flush the pressurizer shell with hot water for | |||
l four to five lours in an attempt to dissolve the crystals and remove | |||
them from the carbon steel surface. To verify that the flushing process | |||
was effective in removing the boron, the licensee planned to collect | |||
water samples hourly at the base of the pressurizer and obtain data on | |||
: boron concentrations, expecting the concentrations to decrease over | |||
l time. The inspector questioned the confidence level of the validation | |||
l | |||
plan as a function of sampling frequency, and asked if an hourly sample | |||
would provide sufficient data to verify that boron concentrations were | |||
. | |||
indeed decreasing over time. The licensee agreed that more frequent | |||
sampling would yield a more robust conclusion and planned to sample the | |||
i flushing water every half hour. The ins)ector reviewed the results of | |||
l | |||
the pressurizer flushing, documented in )IP 2-C97-0952. and concluded | |||
that the flushing plan was effective in removing any dried boric acid | |||
! | |||
from the pressurizer shell. | |||
c. Conclusions | |||
The inspector concluded that documentation for the modification of the | |||
Unit 2 pressurizer manway was satisfactory and engineering | |||
considerations for modification, inspection, and cleaning of the | |||
pressurizer shell were very good. Results of the boric acid cleanup | |||
indicated that the plan had been effective. | |||
E2.2 Desian Control | |||
a. Ir;soection | |||
r Scope (37550) | |||
The inspector reviewed modifications being implemented during the Unit 2 | |||
outage. A)plicable regulatory requirements included Regulatory Guide | |||
1.64 and AiSI N45.2.11-1974. Quality Assurance Requirements for the | |||
Design of Nuclear Power Plants 10 CFR 50.59,10 CFR 50 Appendix B the | |||
. licensee's Quality Assurance Topica'l Report (Duke-1-A), and associated | |||
l | |||
I | |||
i | |||
; | |||
Enclosure 2 | |||
' | |||
. | |||
. | |||
24 | |||
: | |||
design control implementing procedures. The following modifications | |||
were reviewed: | |||
. VN 8303H Replacement of Limitorque Motors on 2NI-54A. 2NI-65B. 1 | |||
2NI-76A. and 2NI-183B | |||
. CN 21377 Modify Safety Injection (SI) Logic to Delete Low Stear ) | |||
Pressure Input 1 | |||
. CN 21375 Upgrade Allowable Temperature for Some Auxiliary Feed | |||
Water (CA) Piping. | |||
l | |||
b. Observations and Findinas ) | |||
1 | |||
The specified post modification testing requirements on the above I | |||
modifications adequately verified the design function of the modified l | |||
equipment. Implementation of the SI signal deletion (CN 21377) resulted I | |||
in damage to six process cards in the Solid State Protection System l | |||
cabinet due to short circuits experienced during wiring terminations. l | |||
The damaged cards were identified during post modification testing. | |||
Appropriate actions were initiated to replace the damaged cards and , | |||
verify the integrity of the remaining installed cards. ' | |||
Replacement Motor Operated Valve Limitorcue motors (VN 8303H) were set ' | |||
up using the VOTES testing procedures anc implementing the applicable GL | |||
89-10 requirements. The modification was required because tie original | |||
size motors for the NI valves were not available. Cracks were found on | |||
the motor shafts' key way of the installed motors. Post modification | |||
verification was accomplished by Quality Control inspections for the CA | |||
piping support modifications to upgrade the allowable piping temperature | |||
(CN 21375). | |||
The 50.59 evaluations for the modifications were adequate. A regulatory | |||
issue was pending on the 50.59 evaluation for the CA piping upgrade (NRC | |||
Inspection Report 50-413.414/96-03). The SI logic signal deletion | |||
safety evaluation was documented in licensing amendments 158 and 150. | |||
c. Conclusion | |||
Regulatory design control requirements were appropriately implemented | |||
for the Unit 2 outage modifications reviewed during this inspection. | |||
E4 Engineering Staff Knowledge and Performance | |||
E4.1 Identification and Correction of Eauioment Problems | |||
; a. Insoection Stone (37550) | |||
The inspector reviewed the licensee's actions related to the | |||
identification and resolution of MOV limitorque motor shaft cracking. | |||
Enclosure 2 | |||
l | |||
l | |||
I | |||
i | |||
' | |||
. | |||
. r | |||
1 | |||
25 | |||
Applicable regulatory requirements included 10 CFR 50 Appendix B and the | |||
licensee's Topical Quality Assurance Program. | |||
b. Observations and Findinas | |||
< | |||
industry experience reports in 1995 and late 1996 noted examples of | |||
< | |||
motor shaft key way cracking in large high speed limitorque MOV motors. | |||
The reports generally indicated the problem occurred in 3600 rpm motors | |||
sized at 80 ft-lbs and larger. There were ten applications identified , | |||
at Catawba which included the four cold leg accumulator isolation valves ) | |||
and the NI-183 valves on each unit. The licensee implemented a motor | |||
shaft inspection into the GL 89-10 program in 1996. No cracks were 1 | |||
identified on the Unit 1 valves inspected during the previous outage. ' | |||
There were cracks identified on three Unit 2 valves inspected during the | |||
current outage. Replacement motors of the original sizes were | |||
unavailable therefore a minor modification was implemented to change | |||
the motor sizes. The original 175 ft-lb motor on 2NI-183B was replaced | |||
with a 150 ft-lb motor from Cold Leg Accumulator valve 2NI-54. The | |||
original 150 ft-lb motors on 2NI-54A. 2NI-65B and 2NI-76A were replaced | |||
with 80 ft-lb. 80 ft-lb. and 100 ft-lb motors, respectively. Valve | |||
motor torque switch settings and parameters were revised to meet the | |||
recuirements of the GL 89-10 program and motor / valve application. | |||
. Adcitionally, the associated motor control center overload heaters were | |||
replaced on each valve to be consistent with the motor protection | |||
requirements. | |||
c. Conclusion 4 | |||
The identification and correction of MOV shaft key way cracking in Unit | |||
2 safety injection system valves was a good example of engineering | |||
identification and resolution of equipment problems. Industry operating | |||
experience was appropriately incorporated into licensee activities and | |||
effectively eliminated a potential safety-related equipment failure ' | |||
mechanism. | |||
E8 Hiscellaneous Engineering Issues (92903) | |||
E8.1 .(flosed) VIO 50-413.414/96-13-04: Inadequate Design Controls - Two | |||
Examples | |||
Example 1-Selection of Main Steam Isolation Valve (MSIV) Solenoid | |||
Valves: This item identified a discrepancy where the nameplate design | |||
rating of MSIV solenoid valves was less than the maximum design pressure | |||
of the instrument air system. The ins)ector reviewed the licensee's | |||
response dated November 6. 1996. The Jnit 1 solenoid valves were | |||
replaced with aapropriate valves prior to identification of the | |||
discrepancy. T1e valve manufacturer certified by letter that the | |||
l | |||
existing Unit 2 solenoid valves were acceptable until replacement at the | |||
i | |||
next refueling outage. The inspector verified that the Unit 2 solenoid | |||
l valves were replaced with upgraded valves during this refueling outage | |||
Enclosure 2 | |||
l | |||
i | |||
' | |||
l . | |||
. | |||
l 26 | |||
' | |||
(MW0s 96070278. 96070289. 96070280. 96070287) and testing of the | |||
replacement solenoid valves was performed satisfactorily (PT | |||
2/A/4200/09. Engineered Safety Feature Actuation Periodic Test). | |||
Examole 2-Standby Shutdown System (SSS) Make-uo Pumn . Calculation - This | |||
item identified calculation design input errors ' 'd to the system | |||
conditions and pulsation damper which were useo 4 | |||
.wify the Net | |||
Positive Suction Head (NPSH) for the SSS make-up pum). The licensee's | |||
November 6. 1996, response to the violation stated tie design inputs for | |||
the SSS make-up pum) sizing calculation and the damper design would be | |||
evaluated and opera]ility for the Unit 1 and 2 pumps verified. The | |||
inspector reviewed the licensee's completed corrective actions and | |||
verified that the in)ut errors were resolved. Additionally, the actions | |||
to assure pump opera]ility were completed. | |||
E8.2 (Closed) DEV 50-413.414/92-01-03.: Breaker Coordination | |||
This deviation was closed based on NRC Inspection Report 50-413.414/96- | |||
19. | |||
E8.3 (Closed) VIO 50-413.414/96-12-03: Inadequate Design Controls For | |||
Ensuring Containment Crane Wall And Floor Drain Screens Implemented | |||
. Design Requirements. l | |||
This item identified containment crane wall penetrations and floor drain i | |||
screens that did not implement design requirements developed to preclude ; | |||
transport of debris to the Emergency Core Cooling System sum) screens. l | |||
The licensee's October 29, 1996. violation response stated tlat the ! | |||
crane wall Jenetrations were filled with cualified foam to preclude any | |||
flow throug1 them and modifications were ceveloped correct the screen | |||
size of the floor drain screens. The inspector reviewed the licensee's j | |||
completed corrective actions, including minor modifications (CNCE-8116. ) | |||
8139. 8186) and drawing revisions (CN-1070-5. rev. 14). The inspector | |||
also performed a walkdown of the unit 2 containment building and | |||
verified that the modifications were installed. | |||
IV. Plant Support | |||
R1 Radiological Protection and Chemistry Controls | |||
R1.1 Tour of Ridioloaical Protected Areas | |||
a. Insoection Scooe (83750. 71750) | |||
The inspectors reviewed implementation of selected elements of the | |||
licensee's radiation protection program as required by 10 Code of | |||
Federal Regulations (CFR) Parts 20.1201. 1208, 1501. 1502. 1601, 1703. | |||
i 1802. 1902, and 1904. The review included observation of radiological | |||
protection activities, including personnel monitoring controls, control | |||
: | |||
Enclosure 2 | |||
_ _ _ _ .__ _ __ _ .. _ . - _ _ _ _ . _ _ _._ _ _ _ . _ _ _ . _ | |||
' | |||
l | |||
P , ; | |||
* | |||
, | |||
> | |||
. | |||
l. | |||
L 27 | |||
of ra'dioactive material, radiological postings, and radiation area /high | |||
radiation area controls, | |||
b. Observations and Findinas | |||
During tours of the Auxiliary Building and radioactive waste ! | |||
storage /handhng facilities. the inspector reviewed survey data and ' | |||
performed selected independent radiation and contamination surveys of | |||
radioactive material storage areas. Observations and survey results | |||
determined-the licensee was effectively controlling and storing | |||
radioactive material. ' | |||
i - - | |||
i | |||
. ~The inspector reviewed records for selected employees who had recently ; | |||
! | |||
worn respiratory protection equipment. The inspector verified that for - < | |||
the records reviewed, each worker had successfully completed respiratory | |||
l protection training, was medically qualified, and was fit-tested for the | |||
l specific respirator type used in accordance with licensee procedural | |||
! requirements. All respiratory protection equipment observed during | |||
facility tours was being maintained in a satisfactory condition. The - | |||
licensee had continued to implement engineering controls for respirator | |||
reductions. | |||
. During plant tours, the inspector observed that Extra High Radiation | |||
, | |||
Areas were locked as required by licensee procedures. The inspector | |||
l also observed dosimetry controls for these areas were also established | |||
E | |||
in Radiation Work Permits (RWPs) as required by licensee procedures. t | |||
The licensee's records indicated that the licensee was maintaining : | |||
approximately 145,000 square feet (ft2 ) of floor space as a | |||
P Radiologically Controlled Area (RCA). Records also showed that the | |||
licensee maintained approximately 800-1000 ft2 (or less than 1 percent) | |||
of the RCA as contaminated area during non-outage periods. During the- | |||
current outage period, the licensee was maintaining approximately 1200 | |||
' | |||
2 | |||
. ft as contaminated area. | |||
t The inspectors reviewed Personnel Contamination Event (PCE) reports | |||
prepared by the licensee to track, trend, determine root cause, and any | |||
necessary followup action. Approximately 49 PCEs had occurred in 1997: | |||
of which, approximately 38 PCEs had occurred during the current Unit 2 | |||
outage. The inspectors reviewed PCE log sheets for the past three years | |||
and noted PCEs continued to trend downward. The licensee attributed | |||
this reduction to several planned contamination control initiatives, | |||
, | |||
.uch as: increased followup with workers following contamination events: | |||
! | |||
reduction of contaminated areas: and reductions in radioactive waste. | |||
During facility tours. the inspectors observed that survey | |||
instrumentation and continuous air monitors observed in use within the | |||
- | |||
! RCA were operable and currently calibrated. The inspectors observed a | |||
survey instrument (portable frisker) in the Unit 2 Reactor Containment | |||
( Building which had not been source checked as required by licensee | |||
Enclosure 2 | |||
t | |||
I | |||
_- . | |||
9= --9 | |||
. _ .~ - - . - .. -. . _ _ , .__ - _ .- | |||
l | |||
' | |||
, | |||
. | |||
28 | |||
- | |||
Procedure HP/0/B1003/22. Paragraph 4.9. The licensee conducted an | |||
immediate investigation and located another frisker in the Unit 2 | |||
Reactor Containment Building which was available for use in the area ! | |||
that had not been source checked. The licensee removed both instruments | |||
from the work area and performed a source check of the instruments to | |||
verify operability. Both instruments source checked satisfactorily. | |||
The licensee also initiated a Problem Investigation Process (PIP) report | |||
to investigate the problem. The inspectors informed the licensee that ; | |||
using survey instruments that had not been source checked was a | |||
violation of licensee procedure and TS 6.8.1. Procedures and Programs. | |||
However, based on the licensee's immediate corrective actions and the | |||
safety significance of the circumstances. this licensee identified and | |||
corrected violation is being treated as a Non-Cited Violation consistent , | |||
with Section VII.B.1 of the NRC Enforcement Policy. NCV 50-413.414/97- | |||
07-04: Failure to Source Check Survey Instruments as Required by | |||
Licensee Procedures. | |||
The ins)ectors reviewed controls for entering the RCA and performing | |||
work. T1ese controls included the use of RWPs to be reviewed and | |||
understood by workers prior to entering the RCA. The inspectors | |||
reviewed selected RWPs for adequacy of the radiation protection | |||
requirements based on work scope, location, and conditions. For the | |||
. RWPs reviewed, the inspectors noted that appropriate protective | |||
clothing and dosimetry were required. During tours of the plant, the | |||
inspectors observed the adherence of plant workers to the RWP | |||
requirements. The inspectors also verified the licensee was effectively | |||
,. managing controls for any declared pregnant women in regards to | |||
embryo / fetus doses as required by 10 CFR 20.1208. The licensee was | |||
, holding current personnel dosimetry accreditation from the National | |||
: Voluntary Laboratory Accreditation Program (NVLAP) as required by 10 CFR | |||
20.1501. | |||
c. Conclusions | |||
Based on observations and procedural reviews, the inspectors determined | |||
the licensee was effectively maintaining controls for personnel | |||
monitoring. respiratory protection, control of radioactive material, | |||
radiological postings, and radiation area /high radiation area controls | |||
as required by 10 CFR Part 20. One NCV was identified for failure to | |||
source check survey instruments as required by licensee procedure. | |||
R1.2 Occuoational Radiation Exoosure Control Proaram | |||
l a. Insoection Scooe (83750) | |||
The inspectors reviewed the licensee's implementation of 10 CFR | |||
;' 20.1101(b) which requires that the licensee shall use, to the extent | |||
practicable, procedures and engineering controls based upon sound | |||
radiation protection principles to achieve occupational doses and doses | |||
, | |||
Enclosure 2 | |||
l | |||
: | |||
l | |||
l | |||
1 | |||
.- _ _ .. . _ _ _ _ _. _. __ _ _ ___ | |||
0 | |||
. | |||
29 | |||
to members of the public that are As Low As Reasonably Achievable | |||
(ALARA). | |||
b. Observations and Findinas | |||
The inspectors review of the licensee's ALARA program determined that | |||
the licensee had established an annual exposure goal of approximately | |||
286 person-rem, which included the Unit 2 outage goal of 132 person-rem | |||
and Jart of a planned Unit 1 outage to begin late in 1997. At the time | |||
of t1e inspection the licensee was tracking approximately 9 person-rem | |||
below previous estimates. The licensee had continued to track and trend | |||
outage exposures for purposes of future outage preplanning and it was | |||
determined that exposures continue to trend downward based on ALARA | |||
initiatives. Several ALARA initiatives reviewed during the inspection | |||
that attributed to lower personnel exposures included: improved | |||
scheduling to optimize the use of shielding and reduce worker congestion | |||
in areas; replacement of stellite valve components with components made | |||
from low to no stellite materials: a successful crudburst during the | |||
Unit 2 shutdown which reduced Unit 2 dose rates by approximately 15 | |||
percent lower than previous Unit 2 outages; increased use of shielding: | |||
and a improved method for workers to initiate ALARA suggestions. | |||
. During tours of the facility the inspectors also observed Radiation | |||
protection (RP) technicians controlling access to work areas to minimize | |||
Personnel exposure and briefing workers in the work areas as | |||
radiological conditions changed. The inspectors also observed personnel | |||
beir.g briefed on ALARA considerations during specific briefings l | |||
conducted to address RWP requirements. | |||
c. Conclusions , | |||
l | |||
Based on licensee planning efforts to reduce source term and the ) | |||
licensee's efforts to achieve established exposure goals which were | |||
challenging, the inspectors determined the licensee was maintaining | |||
programs for controlling exposures ALARA and continued to be effective | |||
j in controlling overall collective dose. | |||
R5 Staff Training and Qualification in Radiation Protection j | |||
a. Insoection Scoce (83750 and 84750) | |||
, | |||
Training was reviewed to determine whether radiation protection | |||
technicians had been instructed in radiation procedures to minimize , | |||
radiation exposures and control radioactive material as required by 10 ' | |||
CFR 19.12. | |||
t | |||
' | |||
b. Observations and Findinas | |||
The inspectors reviewed training requirements for RP technicians and the 4 | |||
continuing training curriculum for the period of January 1,1996. | |||
Enclosure 2 | |||
! | |||
l | |||
l | |||
- | |||
_ __ | |||
' | |||
. | |||
. | |||
30 | |||
through April 5, 1997, which included industry events and topics to | |||
minimize radiation exposure. The inspectors also interviewed RP | |||
personnel and observed work practices to determine the effectiveness of | |||
continuing training. i | |||
c. Conclusions | |||
Based on the training activities reviewed, the inspectors determined | |||
radiation protection technicians were receiving an appropriate level of l | |||
training to perform routine work activities involving radiation and/or | |||
radioactive material. | |||
R7 Quality Assurance in Radiation Protection and Chemistry | |||
a. Insoection Scooe (83750) | |||
: | |||
10 CFR 20.1101 requires that the licensee periodically review the RP | |||
program content and implementation at least annually. Licensee periodic | |||
reviews of the RP program were reviewed to determine the edequacy of l | |||
identification and corrective actions. ' | |||
b. Observations and Findinas | |||
. | |||
By reviewing RP procedures, observing work, reviewing industry | |||
documentation, and performing plant walkdowns to include surveillance of | |||
work areas by supervisors and technicians during normal work coverage, i | |||
the inspector determined that Quality Assurance audits and Self- l | |||
Assessment efforts in the area of RP were accomplished. Documentation | |||
of problems by licensee representatives was included in Quality | |||
Assurance Audits and Self-Assessment Reports. Corrective actions were | |||
included in the licensee's Problem Investigative Process and were being | |||
completed in a timely manner. | |||
During the inspection, the inspector reviewed the licensee's self- | |||
assessment processes for evaluating an event in which unsuspected resin | |||
was found in the 2B containment spray heat exchanger on April 10, 1997. | |||
The resin was analyzed by gamma isotopic analysis and determined to be | |||
mixed bed resin. The licensee began immediate followup actions to | |||
determine the extent of a Jotential spread of resins into plant systems | |||
that could be affected. T1e licensee formed a Failure Investigation | |||
Process Team to determine the source of the resin and to develop a | |||
recovery plan. The team was divided into key areas to identify the root | |||
cause, evaluate sluicing operations and alignments that could affect the | |||
potential spread of resin, identify potentially degraded ecuipment. | |||
identify components that could be potentially impacted, anc develop a | |||
, | |||
' | |||
cleanup plan. The licensee's investigation revealed that the probable | |||
source of the resin was a potential tear in a screenwire used to contain | |||
! mixed resin inside of an ion exchanger. The ion exchanger is used | |||
i | |||
' | |||
during spent fuel pool cleanup evolutions. The licensee determined that | |||
only a small amount of resin was present in the containment spray | |||
Enclosure 2 | |||
1 | |||
. | |||
! | |||
( i l | |||
l -. : | |||
' | |||
L | |||
i | |||
31 | |||
l | |||
l system, and cleanup actions were initiated to remove the resin that had l | |||
1 | |||
o | |||
been identified. A total of approximately 200 - 250 milliliters of | |||
resin was removed from the spent fuel pool purification and containment ! | |||
< | |||
spray systems. The licensee initiated actions to clean out ion 6 | |||
l exchanger post filter housings whenever filters are changed to help i | |||
l eliminate the potential for the small amounts of resin from entering l | |||
l | |||
' | |||
into the containment s] ray system. The licensee's engineering ; | |||
evaluation concluded tlat there were no operability concerns resulting . | |||
i from this event, and the inspector concluded that the licensee's review | |||
l for operability was logical. The inspector determined that the licensee ! | |||
! | |||
was aggressive in performing a root cause analysis of the resin event. ! | |||
l and the licensee's assessments of the event were good. i | |||
! | |||
c. Conclusions i | |||
! | |||
The inspector determined the licensee was performing Quality Assurance ! | |||
Audits and effectively assessing the radiation protection program as ! | |||
required by 10 CFR Part 20.1101. The inspector also determined the : | |||
licensee was completing corrective actions in a timely manner. | |||
l | |||
F2 Status of Fire Protection Facilities and Equipment | |||
'. | |||
' | |||
F2.1 00erability of Fire Protection Facilities and Ecuioment | |||
f | |||
a. Inspection Scoce (64704) i | |||
i | |||
' | |||
The inspectors reviewed open corrective maintenance work orders on fire | |||
protection components and operation's list of out-of-service fire | |||
protection equipment to assess the licensee's performance for returning | |||
degraded fire protection components to service. In addition, walkdown ! | |||
inspections were made to assess the material condition of the plant's l | |||
fire protection systems, equipment, features and fire brigade equipment. t | |||
b. Observations and Findinos ! | |||
Maintenance and Ooerability of Fire Protection Ecuioment and Comoonents | |||
l | |||
As of March 31, 1997, there were approximately 22 fire protection ) | |||
related work requests-in which the work had not been completed. Most of ' i' | |||
these involved minor corrective maintenance work items and did not | |||
! | |||
affect the operability of the components. All of these work requests. i | |||
except for work request item 910001140, were initiated in 1997 or late | |||
: 1996. Item 910001140 involved repairs to the fire pump suction screens | |||
! | |||
which were to be corrected by minor modification CE-3197. This work had | |||
been completed except for the proper reinstallation of the suction | |||
screens. As of the date of this inspection, these screens had not been , | |||
i fully installed to the botsom of the screen frame. This resulted in an ! | |||
estimated area approximately 78x11 feet in size near the bottom of the | |||
pump suction pit not being filtered. | |||
i | |||
: | |||
l | |||
Enclosure 2 | |||
! | |||
! | |||
' | |||
, | |||
. | |||
._ - - .- - . | |||
. l | |||
. | |||
. | |||
32 | |||
Two of the three fire pumps take suction from the fire protection | |||
suction pit. This suction pit was provided with two suction screens | |||
with 3/8-inch mesh installed to filter and prevent raw lake water trash | |||
and debris from entering the suction pit for the pumps and clogging the | |||
suction inlets for the two pumps. The third fire pump takes suction | |||
from the suction pit for the low pressure service water pumps. | |||
The fire pump suction screens were found degraded in late 1990 and | |||
repairs were initiated in 1991. Following these repairs. the suction ' | |||
screens were not properly reinstalled. Reportedly, a lifting beam | |||
device was misplaced during the modification process. Without the beam | |||
device the filters could not be properly installed. The Catawba Fire | |||
Protection OA Program has been incorporated into the Duke Topical Report | |||
GA Program as OA Condition 3. The Topical Report. Section 17.3.1.6 | |||
states that Duke has established a corrective action process whereby all i | |||
personnel are to assure conditions adverse to quality are promptly | |||
identified, controlled, and corrected. Also. Topical Report Section | |||
17.3.2.13 - Corrective Action. requires conditions adverse to quality to | |||
be corrected The failure to correct the degraded filter screens for | |||
the fire pumps in a timely manner is identified as Violation 50- | |||
413.414/97-07-05. Following this inspection, the licensee notified the | |||
inspectors that these screens were properly installed on May 14. 1997. | |||
. | |||
Otherwise, the inspectors concluded that there was no significant | |||
maintenance backlog associated with fire protection components. | |||
Also, as of March 31. 1997, there were 22 degraded or inoperable fire | |||
protection components. Most of these items were related to the Unit 2 | |||
refueling outage which was in progress. For example several fire | |||
barrier penetrations were open for movement of materials through open | |||
floor hatches and the CO2 system for the 2A diesel generator was removed | |||
from service due to maintenance work being performed on the diesel | |||
engine. The remaining degraded features were either in nonsafety- | |||
related areas or were minor discrepancies which did not affect the ! | |||
operability of the system or component. Four of these items had been l | |||
degraded since late 1996. the remainder had been degraded since early i | |||
1997 The inspectors verified that appropriate com)ensatory measures i | |||
had been implemented for the degraded components, w1ere required. One I | |||
degraded component required a continuous fire watch and three degraded ' | |||
components required an hourly fire watch patrol. The remaining degraded I | |||
components were considered operable and did not require any compensatory | |||
actions. l | |||
' | |||
The inspectors toured the plant and noted that the operable fire | |||
; protection systems were well maintained and the material condition was | |||
; very good. | |||
l | |||
Enclosure 2 | |||
l | |||
_ . . ~ _ __ _ . _ _ _ _ , _ _ _ _ _ . _ _ _ - | |||
' | |||
. | |||
. | |||
33 | |||
i | |||
Fire Briaade Eauioment: ! | |||
The fire brigade turnout gear was stored in a fire brigade equipment | |||
building adjacent to the Unit 2 Turbine Building. A sufficient number , | |||
of turnout gear, consisting of coats, Sants boots, helmets, etc., was ! | |||
provided to equip the fire brigade mem)ers expected to respond in the i | |||
event of a fire or other emergency. The equipment was properly stored ' | |||
and well maintained. | |||
c. Conclusions | |||
The low number of open maintenance work orders and degraded fire | |||
protection components, in conjunction with the good material condition | |||
of the fire protection components and fire brigade equipment, indicated | |||
that, in general, appropriate em)hasis had been placed on the | |||
maintenance and operability of tie fire protection equipment and | |||
components. | |||
The work to repair the suction screens for two of the three fire pump's | |||
suction piping had been o)en since 1991 and was not complete. The lack | |||
of prompt resolution of t1e work was identified as a violation. | |||
. | |||
F2.2 Surveillance of Fire Protection Features and Eauioment | |||
a. Insoection Scone (64704) | |||
The inspectors reviewed the following completed surveillance and test | |||
procedures: | |||
- | |||
IP/0/A/3350/13. Revision Change 0 Retype 5. EFA System Detector | |||
Test Procedure, Data Gathering Panel 10. Completed January 20, | |||
1997. | |||
- | |||
IP/0/A/3350/16. Revision Change 0 Retype 2. EFA System Detector | |||
Test Procedure, Data Gathering Panel 13. Completed February 6. | |||
1997. | |||
- | |||
PT/0/A/4400/01A, Revision Change 0 Retype 32. Exterior Fire | |||
Protection Functional Capacity Test. Completed January 29, 1996. | |||
- | |||
PT/0/A/4400/01S, Revision Change 0 Retype 25. Exterior Fire | |||
Protection System - Raw Water Yard (RY) Fire Protection Flow | |||
(Underground) Periodic Test. Completed April 9.1996 and December | |||
5, 1996. | |||
The frecuency of selected surveillance test procedures were also | |||
reviewec, | |||
i | |||
Enclosure 2 | |||
. . _ . __ . _ _ _ _ . _ _ _ __ | |||
l | |||
4 | |||
. | |||
34 l | |||
l | |||
b. Observations and Find 1nas | |||
The completed fire protection surveillance tests reviewed by the | |||
inspectors had been appropriately completed and met the. acceptance ; | |||
criteria. The test procedures were well written and met the fire ! | |||
3rotection surveillance requirements of FSAR Chapter 16.9. Selected ; | |||
_icensee Commitments (SLC). The surveillance procedures for the ; | |||
capacity tests on the fire pumps required test data for multiple points j | |||
on the pump curve to be obtained. This data provided good verification l | |||
of the pump's performance. | |||
During the review of Surveillance PT/0/A4400/01A. the inspectors noted l | |||
that the October 1995 surveillance test indicated that the water flow | |||
through the piping system would not deliver adequate fire flows This | |||
test is conducted every three years and measures the flow of water ; | |||
through various sections of piping to determine if the system will ' | |||
provide an adequate flow path from the fire pumps to the various i | |||
sprinkler and hose stations located in the plant to meet the required l | |||
design head 3ressure and volume requirements. Following the October | |||
1995 test, t1e system was extensively flushed and retested in April i | |||
1996. This test found that the system remained deficient. The flow | |||
tests were performed by isolating the normal loop piping such that the | |||
. flow tests were through a single pipe. The system would provide the | |||
required design flow rates as long as the loop flow paths were | |||
maintained in service. ; | |||
The licensee developed a major pipe cleaning and flushing project | |||
utilizing the " hydro-lase" process which was performed by station | |||
personnel working under the supervision and coordination of a vendor | |||
specialist. During the pipe cleaning activities several automatic | |||
sprinkler systems and hose stations were required to be removed from | |||
service. The licensee coordinated this work to require a minim;m number ; | |||
of systems to be inoperable at any one time. Appropriate compensatory l | |||
actions, consisting of a fire watch with backup fire suppression, were ; | |||
provided as remedial actions while the required fire suppression systems ' | |||
were inoperable. Based on the review of the work activities and | |||
interviews with the plant staff, the inspectors concluded that good | |||
coordination and oversight of these activities were provided. Following | |||
completion of the pipe cleaning activities the underground piping was | |||
retested in December,1996 and was found to be capable of delivering the | |||
required fire flow. | |||
The surveillance requirements for the fire protection systems were | |||
contained in FSAR Chapter 16.9. The results of the inspector's review | |||
I of these features is located in Section F3. | |||
l | |||
c. Conclusions | |||
l | |||
Good surveillance and test procedures were provided for the fire | |||
protection systems and features. Procedure implementation was | |||
Enclosure 2 | |||
! | |||
l | |||
1 | |||
_ . _ . ._ _ __ - __ . ._ _- ___ _ _.__. | |||
' | |||
I o | |||
. | |||
35 | |||
effective. The coordination of the fire protection water piping | |||
cleaning project was excellent. | |||
F3 Fire Protection Procedures and Documentation | |||
a. Insoection Scooe (64704) | |||
The inspectors reviewed the following procedures for compliance with the | |||
NRC requirements and guidelines: | |||
- | |||
Nuclear Station Directive 112. Revision 0. Fire Brigade | |||
Organization. Training and Responsibilities | |||
- | |||
Site Directive 2.12.5, Revision 3. Control of Combustible | |||
Materials Within the Protected Area | |||
- | |||
Site Directive 2.12.6. Revision 3. Fire Protection. Detection and | |||
Barrier Impairment Reporting | |||
- | |||
Site Directive 2.12.7. Revision 4. Fire Protection / Detection ! | |||
! Remedial Actions | |||
!. | |||
- | |||
Site Directive 3.3.9. Revision 1. Hot Work Authorization | |||
: - | |||
FSAR Chapter 16.9. (Revision dated 1/30/96). Auxiliary Systems | |||
(Fire Protection Systems) | |||
- | |||
Prefire Plans. Revision 6. Catawba Prefire Plans 6.1d Procedures | |||
Plant tours were also performed to assess procedure compliance. | |||
b. Observations and Findinas | |||
The above procedures were the principle procedures issued to implement | |||
the facility's fire protection program. These procedures contained the | |||
requirements for program administration. controls over combustibles and | |||
i ignition sources, fire brigade organization and training, and | |||
o)erability requirements for the fire protection systems and features. | |||
, | |||
T1e procedures were well written and met the licensee's commitments to | |||
! | |||
the NRC. | |||
The inspectors performed plant tours a"d noted that, even though the l | |||
plant was in a refueling outage, implementation of the site's fire ! | |||
l prevention program for the control of ignition sources, transient ; | |||
l combustibles, and general housekeeping was good. The accumulation of j | |||
l | |||
t | |||
transient combustible materials and the number of maintenance activities ' | |||
in process due to the refueling outage were-more than anticipated during | |||
normal plant operations. However, appropriate fire prevention controls | |||
were being applied to these activities. | |||
! | |||
Enclosure 2 | |||
i | |||
( | |||
. ._ . ___ _. . ._ . _ . _ ._ __ | |||
l | |||
' | |||
. | |||
, | |||
. | |||
36 | |||
FSAR Chapter 16.9. Selected Licensee Commitments. Auxiliary Systems | |||
(Fire Protection Systems) provides the operability and surveillance | |||
requirements for the fire protection systems and components. The | |||
inspectors compared these requirements to the requirements which were | |||
formerly in the TS. These requirements remained essentially the same, | |||
except for the following testing frequency changes: fire detectors. | |||
from monthly to annually; fire protection valve alignments, from monthly | |||
: to quarterly; and hose station inspection, from monthly to quarterly. | |||
The licensee had recently changed these surveillance inspection | |||
, | |||
frequencies based on satisfactory results from performance based | |||
l evaluat wis of these systems. The inspectors verified that appropriate , | |||
l 10 CFR 50.59 safety evaluations had been performed for these revisions. l | |||
The trending data on the performance based surveillance inspections were ! | |||
reviewed and indicated that the reliability of these systems was greater l | |||
than 99 percent. This substantiated the changes made to the ! | |||
surveillance frequency requirements. The operability requirements in | |||
the SLC were adequate. However, the water supply and fire detection | |||
systems were the only systems which had time limits established for | |||
restoring inoperable components to operable status. This issue is being | |||
evaluated further by the NRC and is identified as an Inspector Followup | |||
Item pending completion of this review. IFI 50-413.414/97-07-06: Time | |||
Limits for Restoration of Inoperable Fire Protection Components. | |||
. | |||
The prefire plans reviewed by the inspectors were found to be | |||
satisfactory. A minor modification was in process to relocate and | |||
remove some of the fire extinguishers presently installed within the . | |||
plant. Also, a standard fire protection water supply system was I | |||
scheduled to be installed by late 1991 for the nuclear service water ' | |||
intake pumping structure. The prefire plans were scheduled to be | |||
revised upon completion of these modifications. In the interim. | |||
controlled copies of the prefire plans had been marked to indicate the | |||
plant changes as they were completed for each plant area. | |||
c. Conclusions | |||
The fire protection program implementing procedures were good and met | |||
licensee and NRC requirements. Implementation of procedures for the | |||
control of ignition sources, transient combustibles, and general | |||
housekeeping was good. An issue regarding time limits for restoration | |||
of inoperable fire protection components will be reviewed further by the | |||
NRC. | |||
F5 Fire Protection Staff Training and Qualification | |||
a. Inspection Scope (64704) | |||
The inspectors reviewed the fire brigade organization and training | |||
program for compliance with the NRC guidelines and requirements. | |||
l | |||
: | |||
I Enclosure 2 | |||
- - - --- - - _. - . - - -. -- . . . .- | |||
. | |||
. | |||
. | |||
! 37 | |||
l | |||
l b. Observations and Findinas | |||
[ : | |||
j The organization and training requirements for the 31 ant fire brigade | |||
were established by Nuclear Station Directive 112. Revision 0. Fire i | |||
Brigade Organization. Training and Res]onsibilities. The fire brigade I | |||
for each shift was composed of a fire arigade leader and at least four | |||
j brigade members from operations and approximately five members from | |||
maintenance. The fire brigade leeder was a senior reactor o]erator i | |||
(SRO) and was normally one of the unit shift supervisors. T1e other | |||
members from Operations were non-licensed plant operators. One of the i | |||
! fire brigade members was normally assigned the duties of fire brigade | |||
safety officer to provide technical and administrative assistance to the | |||
fire brigade leader and to hel) cssure the safe performance of each fire | |||
l brigade member by checking eac1 member for appropriate dress out prior | |||
l to entering the fire area, maintaining records of each fire brigade , | |||
l | |||
exposure to fire or radiatinn hazards, use of self contained breathing l | |||
apparatus, and reviewing the prefire plans during the emergency for ' | |||
assurance that appropriate measures are being followed for compliance | |||
l ' | |||
with applicable safety and fire hazards in the area. Assignment of a | |||
l fire brigade safety officer was identified as a program strength. | |||
l | |||
Each fire brigade member was required to receive initial, quarterly and | |||
. | |||
annual fire fighting related training and to satisfactorily complete an | |||
annual medical evaluation and certification for participation in fire | |||
brigade fire fighting activities. In addition each member was required | |||
i to participate in at least two drills per year. | |||
. | |||
As of the date of this inspection, there were a total of 34 operations | |||
trained fire brigade leaders and 73 operations personnel and 29 | |||
maintenance personnel on the plant's fire brigade. Approximately 6 fire | |||
brigade leaders.12 operations fire brigade members and 5 mintenance | |||
fire brigade members were assigned to each of the five operations crews. | |||
This was a sufficient number of personnel to meet the facilities fire | |||
brigade procedure requirements for one team leader and nine members per | |||
l shift. | |||
The inspectors reviewed the training and medical records for the fire | |||
brigade members and verified that the training and medical records were I | |||
up to date. The facility utilized off-site qualified state certified | |||
fire brigade training instructors and a state fire training facility to | |||
perform the annual fire brigade training and practical fire training | |||
, | |||
i | |||
scenarios. | |||
During this inspection, the inspectors witnessed a fire brigade drill | |||
involving a simulated fire in an electrical motor for a component | |||
cooling pump located on the 560 foot elevation of the auxiliary | |||
building. The response of the fire brigade to the simulated fire was | |||
; excellent. The brigade leader's direction and fire brigade members' | |||
i | |||
performance, especially the safety officer, were outstanding. A | |||
. | |||
! Enclosure 2 | |||
, | |||
l | |||
_ _ | |||
' | |||
, , | |||
. | |||
l 38 | |||
critique to discuss the brigade performance and future enhancements was | |||
' | |||
, held following the drill. | |||
c. Conclusions | |||
The fire brigade organization and training met the requirements of the | |||
site procedures. Performance by the fire brigade during a drill was | |||
excellent. The use of the fire brigade safety officer position during | |||
fire emergencies was identified as a program strength. | |||
F6 Fire Protection Organization and Administration | |||
i | |||
a. Insoection Scooe (64704) | |||
] | |||
The licensee's managemerit and administration of the facilities fire l | |||
protection program were reviewed for compliance with the commitments to | |||
the NRC and to current guidelines. ) | |||
b. Observations and Findinas | |||
The Civil. Electrical. Reactor. Nuclear Engineering Manager was assigned | |||
the responsibility for implementing the facility's fire protection | |||
,. program. An engineer was assigned the task of coordinating the entire | |||
fire 3rotection program and for coordinating the maintenance, | |||
opera)ility and modifications on the fire suppression systems, fire | |||
barriers, and fire barrier penetrations. Another engineer was i | |||
responsible for coordinating the maintenance, o)erability and ! | |||
modifications on the fire detection systems. T1e Manager of Safety l | |||
Assurance was responsible for providing appropriate training for the i | |||
facility fire brigade and for providing guidance and support in the ' | |||
implementation of the facility's fire protection program. Support on | |||
generic fire 3rotection issues was provided to the site by an engineer | |||
assigned to t7e Corporate Nuclear Engineering Division. | |||
A corporate Fire Protection Business Excellence Steering Team (BEST). | |||
composed of representatives from each of the three Duke nuclear plants | |||
and the corporate staff, was meeting monthly to discuss fire protection | |||
issues and im)rovements needed to enhance the fire protection program at | |||
each site. T1e inspectors reviewed the minutes for the first three | |||
meetings in 1997 and noted a number of issues were under consideration | |||
which, if im)lemented should improve the overall fire protection | |||
program at t1e Duke facilities. The inspector concluded that these | |||
meetings were a positive element of the facility's fire protection | |||
program. | |||
c. Conclusions | |||
- | |||
Strong coordination and oversight were provided over the facility's fire | |||
protection program. The Fire Protection BEST was a positive factor in | |||
Enclosure 2 | |||
i | |||
i | |||
-- . . . . . - _ _ - -- - - _ . _ - . | |||
' | |||
g .. | |||
. | |||
39 | |||
l | |||
I | |||
the identification of potential problems and in the development and | |||
implementation of enhancements to the fire protection program. | |||
l | |||
F7 Quality Assurance in Fire Protection Activities | |||
! | |||
l a. Insoection Scooe (64704) | |||
The following audit report was reviewed: | |||
- | |||
Audit SA-95-24(CN)(RA). Triennial Fire Protection Audit conducted | |||
May 15 through June 8, 1995 | |||
b. Observations and Findinas | |||
Audit SA-95-24(CN)(RA) was a triennial 0A audit of the facilities' fire | |||
protection program. The licensee informed the inspectors that this was | |||
the only comprehensive audit of the fire protection program performed | |||
since Duke's December 18, 1991, request to use performance based | |||
criteria for establishing auoit frequencies was approved by the NRC.'s | |||
letter dated May 7. 1992. Previously, the TS had required annual, | |||
biannual and triennial audits of the fire protection program. However, | |||
based on the licensee's assessment of good fire protection performance. | |||
. only this one triennial audit had been performed at Catawba in recent | |||
years. | |||
TS 6.5.2.9 identified a number of site audits which were performed under | |||
the cognizance of the Nuclear Safety Review Board. The licensee's | |||
December 18, 1991, letter indicated that the audit frequency for all of | |||
these audits were deleted from the TS. and the OA Topical report was to | |||
be revised to indicate that the " audits of selected aspects of | |||
operational phase activities are performed with a frequency commensurate | |||
with safety significance and in such a manner as to assure that an audit | |||
of all safety related functions is completed within a period of two | |||
years." The OA topical report was revised, but only requires an audit | |||
of all "0A Condition 1 functions" to be completed within a period of two | |||
years. Many of the audit items listed by TS Section 6.5.2.9 are | |||
classified as OA Condition 2 or 3 functions. The specified time for | |||
these audits are not listed in the OA topical report. The inconsistency | |||
of not providing a specified frequency for Condition 2 and 3 functions | |||
is being further reviewed by the NRC and is identified as Inspector | |||
Follow-up Item pending completion of this review. 50-413.414/97-07-07: | |||
Audit Frequency Requirements for Activities other than OA Condition 1 | |||
Functions. | |||
The inspectors reviewed the audit findings from the 1995 OA report and | |||
the corrective actions taken on the identified discrepancies. The | |||
report indicated that a comprehensive audit had been performed with nine | |||
findings identified. The corrective action on each finding had been | |||
completed in a timely manner. | |||
l | |||
l Enclosure 2 | |||
k 2.m | |||
I | |||
s .. ' | |||
. | |||
40 | |||
c. Conclusions | |||
The 1995 audit and assessment of the facility's fire protection program | |||
was comprehensive and appropriate corrective action was promptly taken | |||
to resolve identified issues. An issue regarding the control of 0A | |||
audit frequencies will be reviewed further by the NRC. | |||
F8 MiscellaneousFireProtectjonIssues | |||
F8.1 Fire Protection Related NRC Information Notices | |||
The inspector reviewed the licensee's evaluation for the following NRC 1 | |||
Information Notices (IN): ' | |||
- | |||
IN 92-18. Potential loss of Shutdown Capacity During a Control | |||
Room Fire | |||
- | |||
IN 92-28. Inadequate Fire Suppression System Testing | |||
- | |||
IN 93-41. One Hour Fire Endurance Tests Results For Thermal | |||
Ceramics. 3M Company FS 195'and 3M Company E-50 Interam Fire , | |||
Barrier Systems I | |||
.. | |||
- | |||
IN 94-28. Potential Problems with Fire Barrier Penetration Seals | |||
- | |||
IN 9--31. Potential Failure of WILCO. LEXAN-Type HN-4-L. Fire Hose | |||
Nozzles | |||
- | |||
IN 94-58. Reactor Coolant Pump Lube Oil Fire | |||
- | |||
IN 95-36. Emergency Lighting | |||
The licensee's evaluations and corrective actions for these ins were | |||
appropriate, except the evaluation documentation for some of the ins did | |||
not fully indicate the results of the evaluations which were actually | |||
performed. | |||
V. Manaaement Meetinos | |||
X1 Exit Meeting Summary | |||
The inspectors ) resented the inspection results to members of licensee | |||
: management at t1e conclusion of the inspection on April 30. 1997. On May 14 | |||
; a teleconference was held between Region II DRS management and licensee | |||
management representatives to discuss the violation included with this report. | |||
l The licensee acknowledged the findings presented. No proprietary information | |||
t | |||
was identified. . | |||
Enclosure 2 | |||
i | |||
- - . . _. _ . _ _ . _ _ _ - _ . . . _ _ _ _ - . _ . - | |||
_ _ . _ _ . _ _ _ _ - . | |||
, | |||
l | |||
" | |||
l ,,-.. , | |||
: | |||
- | |||
: | |||
l 41 | |||
l i | |||
l | |||
l | |||
l | |||
l | |||
' | |||
PARTIAL LIST OF PERSONS CONTACTED | |||
Licensee | |||
Bhatnager, A., Operations Superintendent | |||
Birch. M., Safety Assurance Manager . | |||
Christopher. S. , Emergency Planning Supervisor ' | |||
l Copp. S Nuclear Regulatory Affairs Manager | |||
' | |||
Coy. S., Radiation Protection Manager i | |||
Forbes. J., Engineering Manager ' | |||
Giles, R. Work Control Inservice Inspection Coordination , | |||
Harrall. T. Instrument and Electrical Maintenance Superintendent ' | |||
: Kelly. C.. Maintenance Manager | |||
! Kimball. D., Safety Review Group Manager | |||
! Kitlan. M., Regulatory Compliance Manager ' | |||
Kulla D. Civil Engineering Supervisor | |||
McCollum W., Catawba Site Vice-President | |||
Nicholson. K., Compliance Specialist | |||
i | |||
J | |||
l Peterson. G., Station Manager | |||
l. Propst. R., Chemistry Manager | |||
Purser, M.. Senior Engineer | |||
, | |||
l l | |||
l Robinson G., Work Control Execution Support | |||
l Rogers D., Mechanical Maintenance Manager i | |||
Tower, D., Compliance Engineer ' | |||
i | |||
( | |||
) | |||
I | |||
! | |||
> | |||
\ | |||
l | |||
1 | |||
l | |||
l | |||
l | |||
, | |||
Enclosure 2 | |||
l | |||
l | |||
i j | |||
.- - - - - . .- | |||
' | |||
7.. | |||
. | |||
42 | |||
INSPECTION PROCEDURES USED | |||
IP 37550: Engineering | |||
IP 37551: Onsite Engineering | |||
IP 40500: Effectiveness of Licensee Controls in Identifying, Resolving, and | |||
Preventing Problems | |||
' | |||
! | |||
IP 49001: Inspection of Erosion / Corrosion Monitoring Programs | |||
IP 61726: Surveillance Observation | |||
IP 62001: Boric Acid Program Prevention Program | |||
IP 62707: Maintenance Observation | |||
, | |||
' | |||
IP 64704: Fire Protection Program | |||
IP 71707: Plant Operations | |||
l IP 71750: Plant Support Activities | |||
' | |||
IP 73753: Inservice Inspection | |||
IP 83750: Occupational Radiation Exposure | |||
l IP 84750: Radioactive Waste Treatment and Effluent and Environmental | |||
Monitoring | |||
IP 92901: Followup - Operations | |||
IP 92902: Followup - Maintenance | |||
IP 92903: Followup - Engineering | |||
ITEMS OPENED, CLOSED, AND DISCUSSED | |||
. | |||
Opened | |||
50-414/97-07-01 VIO OPEN Inadequate Procedure Resulting in | |||
Loss of Spent Fuel Pool Cooling with | |||
Core Off-loaded. (Section 01.1) | |||
50-413,414/97-0? 32 1FI OPEN Boron Dilution Mitigation System | |||
Reliability Resolution. (Section | |||
01.4) | |||
50-413.414/97-07-03 IFI OPEN Review Corrective Actions For | |||
Storage and Handling Assessment | |||
Findings. (Section M1.2) | |||
50-413,414/97-07-04 NCV OPEN Failure to Source Check Survey | |||
Instruments as required by licensee | |||
procedure. (Section R1.1) | |||
50-413.414/97-07-05 VIO OPEN Failure to Repair Degraded Suction | |||
Screen Filters for Fire Pumps in a | |||
Timely Manner. (Section F2.1) | |||
50-413,414/97-07-06 IFI OPEN Time Limits for Restoration of | |||
, | |||
Inoperable Fire Protection | |||
Components. (Section F.3) | |||
l | |||
j Enclosure 2 | |||
_.. _ _ _ . _ _ . _ _ _ . . _ . _ . . . - . . - . - _ _ _ _ . . _ . . _ . _ _ . . . _ _ _ | |||
: | |||
3..* | |||
. | |||
43 | |||
50-413.414/97-07-07 IFI OPEN Audit Frequency Requirements for | |||
Activities other than OA Condition 1 | |||
Functions. (Section F.7) : | |||
Closed | |||
50-413.414/94-13-01 VIO CLOSED Failure to follow Procedure NSD 703 | |||
and Station Directive 34.0.5 | |||
requirements. (Section 08.1) | |||
l 50-413/95-07-01 VIO CLOSED Inadequate Modification Procedure ! | |||
Resulting in Loss of RHR. (Section , | |||
i | |||
08.2) | |||
50-413.414/95-07-02 VIO CLOSED Inadequate Valve Verification | |||
Activities - Two Examples. (Section | |||
08.3) | |||
50-413.414/96-13-04 VIO CLOSED Inadequate Design Controls (MSIV | |||
Solenoid Valves). Standby Shutdown | |||
System Makeup Pump Sizing | |||
Calculation (Section E8.1) | |||
. | |||
50-413.414/92-01-06 DEV CLOSED Breaker Coordination (Section E8.2) | |||
50-413.414/96-12-03 VIO CLOSED Inadequate Design Controls For | |||
Ensuring Containment Crane Wall and | |||
Floor Drain Screens Implemented | |||
Design Requirements (Section E8.3) | |||
l Enclosure 2 | |||
_ _ , _ | |||
I | |||
, | |||
' | |||
g.. | |||
6 | |||
. | |||
44 | |||
l | |||
l LIST OF ACRONYMS USED | |||
l | |||
ALARA - As Low As Reasonably Achievable | |||
ANSI - | |||
American Nuclear Standards Institute | |||
ASME - American Society of Mechanical Engineers | |||
, | |||
' | |||
BDMS - Boron Dilution Mitigation System | |||
CA - | |||
Auxiliary Feedwater (system) | |||
CHEC - Designation for EPRI computer code | |||
CFR - | |||
Code of Federal Regulations | |||
DEV - | |||
Deviation | |||
DG - | |||
Diesel Generator | |||
DPC - | |||
Duke Power Company | |||
EFA - | |||
Fire Detection System | |||
EPRI - | |||
Electric Power Research Institute | |||
ESS - | |||
Electric System Support | |||
FAC - | |||
Flow Accelerated Corrosion | |||
FME - | |||
Foreign Material Exclusion | |||
FSAR - Final Safety Analysis Report | |||
FWST - Refueling Water Storage Tank | |||
2 | |||
ft - | |||
Square Feet | |||
ft-lb - foot-pounds (force) | |||
GL - | |||
Generic Letter | |||
. IFI - | |||
Inspector Followup Item | |||
IN - | |||
Information Notice | |||
IR - | |||
Inspection Report | |||
ISI - | |||
Inservice Inspection | |||
MOV - | |||
Motor Operated Valve | |||
MSIV - Main Steam Isolation Valve | |||
NCV - | |||
Non Cited Violation | |||
NDE - | |||
Nondestructive Examination | |||
NI - | |||
Nuclear Safety Injection (system) | |||
NSD - | |||
Nuclear System Directive | |||
NSM - | |||
Nuclear Station Modification | |||
NRC - | |||
Nuclear Regulatory Commission | |||
OAC - | |||
Operator Aid Computer | |||
PCE - | |||
Personnel Contamination Event | |||
PIP - | |||
Problem Investigation Process | |||
PORV - Power Operated Relief Valve | |||
psig - Pounds Per Square Inch Gauge | |||
QA - | |||
Quality Assurance | |||
RCA - | |||
Radiologically Controlled. Area | |||
RCP - | |||
Reactor Coolant Pump | |||
RCS - | |||
Reactor Coolant System | |||
RHR - | |||
Residual Heat Removal | |||
RP - | |||
Radiation Protection | |||
rpm - | |||
revolutions per minute | |||
RWP - | |||
Radiation Work Permits | |||
SG - | |||
Steam Generator | |||
SI - | |||
Safety Injection | |||
l SLC - | |||
Select Licensee Commitments | |||
' | |||
Enclosure 2 | |||
. | |||
* | |||
a.- | |||
s | |||
. | |||
45 | |||
SSS - | |||
Standby Shutdown System | |||
TEPR - Top Equipment Problem Resolution | |||
TS - | |||
Technical Specifications | |||
UFSAR - Updated Final Safety Analysis Report | |||
VIO - | |||
Violation | |||
VN - | |||
Variation Notice | |||
WO - | |||
Work Order | |||
. | |||
i | |||
l | |||
I | |||
! | |||
, | |||
i | |||
Enclosure 2 | |||
l | |||
l | |||
: | |||
}} |
Latest revision as of 08:24, 27 October 2020
ML20148F944 | |
Person / Time | |
---|---|
Site: | Catawba |
Issue date: | 05/23/1997 |
From: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
To: | |
Shared Package | |
ML20148F917 | List: |
References | |
50-413-97-07, 50-413-97-7, 50-414-97-07, 50-414-97-7, NUDOCS 9706050102 | |
Download: ML20148F944 (50) | |
See also: IR 05000413/1997007
Text
^
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! U.S. NUCLEAR REGULATORY COMMISSION
REGION II
Docket Nos: 50-413, 50-414
License Nos: NPF-35 NPF-52
Report Nos.: 50-413/97-07. 50-414/97-07
i
Licensee: Duke Power Company
Facility: Catawba Nuclear Station Units 1 and 2
Location. 422 South Church Street
Charlotte. NC 28242
Dates: March 23 - April 26,1997
Inspectors: R. J. Freudenberger, Senior Resident Inspector
P. A. Balmain, Resident Inspector
R. L. Franovich. Resident Inspector
.
R. A. Gibbs, Resident Inspector (In Training)
J. L. Coley, Jr. . Reactor Inspector (Sections M2, E2.1)
D. B. Forbes, Radiation Specialist (Sections R1, R5, R7)
W. H. Miller, Jr.. Reactor Inspector (Sections 08.1, F2,
F3. FS, F6. F7 F8)
R. L. Moore, Reactor Inspector (Sections E2.2, E4.1, E8.1.
E8.2)
Approved by: C. A. Casto, Chief
Reactor Projects Branch 1
Division of Reactor Projects
i
l
1
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j
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Enclosure 2
9706050102 970523
PDR ADOCK 05000413
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EXECUTIVE SUMMARY
Catawba Nucleer Station. Units 1 & 2 4
NRC Inspection Report 50-413/97-07. 50-414/97-07 '
This integrated inspection included aspects of licensee operations. !
maintenance, engineering, and plant support. The report covers a 6-week
period of resident ins)ection: in addition. it includes the results of
announced inspections ay regional reactor safety inspectors. l
Operations
. A Unit 2 loss of spent fuel pool cooling, which was caused by an
inadequate containment penetration test procedure, was identified as a
violation. Other barriers that could have prevented the event included l
increased emphasis on the importance of the system function during the l
pre-job brief and more diligent control board monitoring. The
operator's performance in response to the event was appropriate. The l
Catawba Safety Review Group evaluation of the event was detailed and I
identified substantive corrective actions. (Section 01.1)
- Midloop Activities were well controlled. Nevertheless, the process for
restoring equipment necessary for gravity flows to the core may not be
ensured by administrative controls. (Section 01.2)
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. The inspector concluded that selected initial conditions for the
compensatory action associated with the main control room pressure i
boundary were satisfied. The inspector further concluded that operator
effectiveness in im)lementing this complex compensatory action was I
challenged by lengtly initial conditions, and the practice of not '
periodically reverifying required initial conditions. (Section 01.3)
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. Problems encountered with the Boron Dilution Mitigation System during
the Unit 2 refueling outage were indicative of historically low
reliability and availability, which caused additional control room
operator workload to compensate for the system's low reliability.
(Section 01.4)
. The inspector concluded that actions by operations and Radiation
Protection personnel in response to the radiation alarm in the fuel
handling building were good. However. foreign material exclusion
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administrative controls were not properly im)lemented by personnel
working in the fuel transfer canal area of t1e fuel handling building.
(Section 01.5)
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. A Unit 1 pressurizer )ower operated relief block valve control circuit
failure occurred whic1 is a potential repeat of a previous 1995 failure.
The licensee has planned appropriate actions to determine the cause of
the control circuit component failure. (Section 01.6)
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Maintenance
. The inspector concluded that, in general, outage-related maintenance
activities were ap]ropriately conducted. Although multiple barriers to
minimizing the risc of human error during reactor coolant pump seal
maintenance were noted, the inspector was unaware of any human
performance problems associated with the work. (Section M1.1)
. The licensee's resolution of long-standing elevated vibration levels
associated with the Unit 2B nuclear service water pump motor was very
good. Deficiencies identified with a spare nuclear service water pump
motor, a previous motor failure, and findings identified by licensee
assessments of warehouse storage and handling practices raised questions
about control and storage of spare motors. The issue is identified as
an Inspector Followup Item and will be reviewed during a future
inspection. (Section M1.2)
- Certification records for nondestructive examination (NDE) personnel,
weld examinations, and NDE examination procedures were in accordance
with Code requirements. (Section M2.1)
. * Review of the eddy current outage plan, equipment setup and acquisition
procedures, personnel and equipment certifications, and observation of
data acquisition activities revealed that required documentation was
available and complete, and data acquisition personnel were
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knowledgeable of the eddy current examination process. (Section M2.2)
+ The licensee has implemented an effective program for the detection of
flow accelerated corrosion in components. This program is based on
recommendations found in recognized industry standards. (Section M2.3)
. The maintenance / work control self-assessment programs effectively
identified areas for improvement and a]propriate corrective actions.
The self-assessments apparently contri)uted to improvement in the
performance of the Maintenance and Work Control organizations. (Section
M7.1)
Enaineerina
. The licensee's actions to replace all control rod assemblies that had
evidence of tip cracking were appropriate. (Section El.1)
- Documentation for the modification of the Unit 2 pressurizer manway was
satisfactory, and engineering considerations for the modification,
inspection, and cleaning of the pressurizer were very good. (Section
E2.1)
- Design controls for Unit 2 outage modifications were consistent with
regulatory requirements. (Section E2.2)
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. The motor shaft key way cracking in large high speed limitorque motor
actuators at-Catawba was an example of good identification and ;
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resolution of equipment problems using the Operating Experience Program. '
(Section E4.1)
L Plant Sucoort
. The licensee was effectively maintaining controls for personnel .
monitoring, control of radioactive material, radiological postings. and J
radiation area /high radiation area controls as required by 10 CFR Part i
20. One Non-Cited Violation was identified for failure to source check
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l survey instruments as required by licensee procedure. (Section R1.1)
[ . The licensee was maintaining programs for controlling exposures As Low I
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As Reasonably Achievable and continued to be effective in controlling '
l overall collective dose. (Section R1.2)
. Radiation protection technicians and radiation workers were receiving an
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appropriate level of training to perform work activities involving )
radiation and/or radioactive material. (Section RS)
L . The licensee was performing Quality Assurance Audits and effectively
- . assessing the radiation protection program as required by 10 CFR Part
20.1101 and completing corrective actions in a timely manner. (Section
l R7)
l. . The low number of open maintenance work orders and degraded fire
protection components, in conjunction with the good material condition
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of the fire protection components and fire brigade equipment, indicated
- that, in general appropriate em3hasis had been placed on the
l maintenance and operability of t1e fire protection equipment and
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components. (Section F2.1)
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.- The work to repair the suction screens for the fire pumps' suction
piping had been ooen since 1991 and was not complete. The failure to.
complete this work in a timely manner was identified as a Violation.
(Section F2.1)
. Good surveillance and test procedures were provided for the fire
protection systems and features with effective procedure implementation.
.The coordination of the fire protection water piping cleaning project
was excellent. (Section F2.2)
! . The fire protection program implementing procedures were good and met
licensee and NRC requirements. Implementation of procedures for the i'
control of. ignition sources, transient combustibles, and general
housekeeping was good. An issue regarding time limits for restoration ;
. of inoperable fire protection components will be reviewed further by the '
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NRC under an Inspector Followup Item. (Section F3)
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The fire brigade organization and training met the requirements of the
site procedures. Performance by the fire brigade during a drill was
excellent. The use of the fire brigade safety officer position used
during fire emergencies was identified as a program strength. (Section
F5)
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Strong coordination and oversight were provided over the facility's fire
protection program. The Fire Protection BEST was a positive force in
the identification of potential problems and in the development and
l implementation of enhancements to the fire protection program. (Section
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F6)
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The 1995 audit and assessment of the facility's fire protection program
was comprehensive and appropriate corrective action was promptly taken
to reso:ve the identified issues. An issue regarding the control of OA
audit frequencies was identified as an Inspector Followup Item will be
reviewed further by the NRC. (Section F7)
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Report Details
Summary of Plant Status
Unit 1 began the ]eriod operating at 100% power and operated at essentially
full power througacut the inspection period.
Unit 2 began the period in cold shutdown (Mode 5) in preparation for the End
of Cycle (EOC8) refueling outage. One scheduled period of reactor coolant
system reduced inventory /midloop began and completed on April 23. Midloop was
entered to support the reactor coolant system vacuum refill evolution. At the
close of the inspection period the Unit had returned to cold shutdown (Mode 5) !
and heatup activities in preparation for unit restart were beginning.
Review of Uodated Final Safety Analysis Reoort (UFSAR) Commitgents
While performing inspections discussed in this report, the inspectors reviewed
the applicable portions of the UFSAR that were related to the areas inspected. l
The inspectors verified that the UFSAR wording was consistent with the i
observed plant practices, procedures, and/or parameters, i
I. Operations
01 Conduct of Operations
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01.1 Loss of Spent Fuel Pool Coolina
a. Insoection Scope (71707)
On April 8. Unit 2 was in a refueling outage with all of the fuel off-
loaded to the spent fuel pool. The Operator Aid Computer was out of '
service for replacement, and alignments for testing of containment
isolation valves in the component cooling water non-essential header
were in progress. Inventory was inadvertently drained from the
component cooling water system over a seventy minute period. until the
low-low level setpoint in the component cooling water surge tanks was
reached. At this level, automatic isolation of the non-essential header
occurred. the drain path was isolated, and cooling flow to the spent
fuel pool heat exchanger and pump motor cooler was isolated. 0]erators
shutdown the pump to prevent overheating, initiated makeup to t1e
component cooling water surge tanks. and closely monitored spent fuel
pool temperature. Spent fuel pool temperature increased to a maximum of
108 F. within the TS limit. while operators determined the cause of the
loss of component cooling water inventory and returned the non-essential
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header to service.
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As a result of the event, the licensee initiated Problem Investigation
Process (PIP) report 2-C97-1090 and initiated a root cause evaluation
that was performed by the Catawba Safety Review Group.
The inspector responded to the site upon notification of the loss of
spent fuel pool cooling: discussed the event with various personnel
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involved; reviewed PT/2/A/4200/01T, Containment Penetration Valve
Injection Water System Performance Test, approved 3/26/97: reviewed data
on component cooling water surge tank level spent fuel pool cooling
pump motor temperatures, and spent fuel pool temperature: and reviewed
the root cause evaluation documented in the referenced PIP.
b. Observations and Findinas
At the time of the loss of spent fuel pool cooling, approximately 19 -
hours were available prior to boiling in the spent fuel pool. Operators I
methodically restored cooling within 1.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />, after identifying the
cause, assessing equipment condition, and realigning the component .
cooling water system. l
The licensee's root cause evaluation considered procedural adequacy.
o]erator performance, ad supervisory oversight of the evolution. In
taese areas, problems were identified and appropriate corrective actions
were delineated.
Procedure PT/2/A/4200/01T, Containment Penetration Valve Injection Water
System Performance Test, included steps for the alignment of four
component cooling water containment penetrations that included valve
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manipulation sequences that were incorrect. The incorrect sequences
caused drain paths to be aligned through the inside containment
penetration vent on all four penetrations. The licensee's evaluation
revealed that the Unit 1 procedure had similar errors. The errors
occurred during a process to convert engineering test procedures into
the operations procedure format. Proposed corrective actions included a
formal validation of the technical adequacy of other procedures that
have been or were to be converted. This procedure inadequacy, which
caused the loss of spent fuel cooling constitutes a Violation (VIO) of
TS 6.8.1. Procedures and Programs, and is identified as VIO 50-414/97-
07-01: Inadequate Procedure Resulting in Loss of Spent Fuel Pool
Cooling with Core Off-loaded.
The licensee's evaluation of operator performance concluded that the
equipment operator that performed the valve alignments appropriately
questioned the high flow rate from the vent valves as they were opened,
but failed to stop and contact su3ervision when this unexpected response
was obtained. Also, the control aoard operators were not timely in
their assessment of an observed increased rate of input to the
containment floor and equipment sump.
The inspector noted that the pre-job brief for performing the
containment Jenetration alignments was incomplete. Personnel conducting
the pre-job arief did not emphasize that the component cooling water
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system was affected by the procedure and was being relied upon for
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cooling the spent fuel pool with the core off-loaded. Also, the control
room operators could have more diligently monitored this system, since
it was performing an important function, and identified the decreasing
level in the component cooling water surge tanks before automatic
, actions occurred. Operations management had similar observations and
l took actions to imarove monitoring of systems performing important
functions during t1e remainder of the outage.
c. Conclusions
l The loss of spent fuel pool cooling was caused by an inadequate ;
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containment penetration test procedure. Other barriers that could have
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prevented the event included increased emphasis on the importance of the
system function during the pre-job brief and more diligent control board
monitoring. The operator's performance in response to the event was
appropriate. The Catawba Safety Review Group evaluation of the event
was detailed and identified substantive corrective actions.
01.2 Preoarations for Midlooo
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a. Insoection Scooe (71707)
l. Near the conclusion of its refueling outage. Unit 2 entered midloo) on
! April 23 for vacuum refill of the Reactor Coolant System (RCS). Tie
i inspector reviewed Generic Letter 88-17. Loss of Decay Heat Removal.
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Catawba Nuclear Site Directive 3.1.30. Unit Shutdown Configuration
Control. Rev. 8. and the operating 3rocedures governing the RCS
, draindown to midloop, operation wit 1 reduced RCS inventory, and vacuum
refill. The inspector conducted control room observations during the !
draindown to midloop and portions of unit operation at midloop.
b. Observations and Findinos
The inspector verified that the requirements delineated in Catawba l
Nuclear Site Directive 3.1.30 were satisfied. Specifically, multiple :
thermocouples were available for temperature monitoring; ultrasonics and
sightglass indications were available for level monitoring: vital power
was available from both offsite sources, as well as two emergency diesel
generators; necessary emergency core cooling equipment was either
operable or available: and the gravity flowpath criteria were satisfied
for midloop operation with low decay heat.
Just prior to reduced inventory operations, the inspector noticed that
valves 2ND-33. Residual Heat Removal (RHR) System Return to the
Refueling Water Storage Tank (FWST). 2FW-27A and 2FW-55B. RHR Pumps 2A
and 2B Suction from the FWST. were available as opposed to operable.
These valves are in the flowpaths of the three gravity feeds to the RCS.
The valves were tagged closed in support of RCS maintenance. The
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inspector questioned the a)proariateness of considering the associated
! flowpaths available with tie RiR and FWST valves closed under a tagout.
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Normal makeup to the reactor coolant system via the chemical and volume
control system was available.
l The inspector inquired about the status of the RHR and FWST valves
during reduced inventory and midloo) operations and determined that.
, although they were tagged closed, t1e Work Control Center filed the tags
l in a prominent location to facilitate equipment restoration in the event
l that these valves were needed to mitigate a loss of RHR.
The inspector reviewed Catawba Nuclear Site Directive 3.1.30 to
determine if administrative requirements were being met. The directive
stated that, for midloop operations with low decay heat load, two ;
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available gravity flowpaths were required. The directive defines i
"available" as "the status of a system, structure or component that is '
in service or can be placed in service in a functional or operable state i
by immediate manual or automatic actuation." The directive considers !
actions taken by operators to clear tags acceptable for restoring ,
equipment to functional or operable status within a reasonable period of l
time.
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The inspector raised a concern to the licensee that, while valves 2FW-
27A. 2FW-55B. and 2ND-33 could possibly be restored to service in a
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reasonable period of time, other components that might be impacted by
the maintenance activity in progress might not be accounted for before ;
the gravity flowpath would be utilized. Hence, points of compromised '
system integrity, which could allow flow to be diverted from the RCS.
might be overlooked and either reduce the assumed flow to the RCS or !
extend the amount of time needed to place the gravity flowpath in
service. Although no such conditions were identified during the midloop
and vacuum refill evolutions, the licensee plans to evaluate Nuclear
Site Directive 3.1.30 to determine if changes are warranted prior to the
next refueling outage.
c. Conclusions
The inspector concluded that the draindown to midloop, midloop
operation, and vacuum refill were conducted without incident. In
general, the licensee implements effective controls for these
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evolutions. However, the inspector questioned the availability of 1
equipment required for gravity flow to the core and expressed concern
that the process for restoring needed equipment may not be sufficiently
controlled.
01.3 Doerator Aid Comouter Installation and Comoensatory Action
a. Insoection Scooe (71707)
l During the Operator Aid Computer (OAC) installation, the inspector
- periodically verified that the Loss of DAC procedure was implemented
l while the OAC was unavailable. The inspector observed an open main
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control room door and reviewed the associated compensatory action.
" Control Room Pressure Boundary." dated March 20. 1997, to verify that
the licensee had satisfied selected initial conditions that allowed the
door to remain open. The inspector also evaluated the licensee's
im)lementation of the compensatory action guidance following receipt of
a Jnit 2 fuel handling building high radiation alarm that occurred on
March 24.
b. Observations and Findinas
During the Unit 2 OAC installation. the OAC was not available for <
l automatic surveillance of numerous plant parameters. As a result, the I
control room operators were required to implement PT/1/A/4600/09. Loss
of Operator Aid Computer, and perform those surveillances manually'on
specified time intervals. The inspector periodically verified that the l
procedure was in use while OAC monitoring was unavailable. Often a l
dedicated reactor operator was available to perform this function.
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although that could not always be accommodated. The inspector
determined that the procedure was in place and being implemented when
required.
l The inspector observed that the Unit 2 control room vital access door
was opened on March 22 and was left open continuously to allow passage
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of a flexible ventilation duct (approx. 12 inch diameter). The duct was
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used to exhaust fumes generated from welding performed to install the
replacement operator aid computer in the Unit 2 main control board
panel. The inspector discussed the compensatory actions with
engineering and operations 3ersonnel to determine if the compensatory
actions would ensure that tie control room would pressurize sufficiently
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to meet control room habitability requirements during design basis
events. Both operations and engineering personnel stated the design
basis for contrM room pressurization and habitability would be met
provided that initic1 conditions of the compensatory action were
satisfied and that the control room door would be manually closed, after
separating a connection in the duct. if certain plant events (e.g..
safety injection signal) were to occur.
The inspector verified that selected initial conditions were satisfied
and found no discrepancies with the plant conditions that existed at the
time of the inspection. The inspector observed, however, that the
initial conditions of the compensatory action were not being
periodically verified to ensure that plant changes since the initial
condition verification on March 22 had not invalidated the assumptions
supporting the compensatory action. Operations personnel informed the
inspector that periodic verification of initial conditions for the
compensatory actions was not required.
l The inspector expressed a concern to the licensee that, because there
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was a high number of initial conditions required for this particular
compensatory action and because of the relatively long duration of the
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replacement operator aid com) uter installation, periodic verification of
initial conditions may have 3een warranted to ensure that necessary
conditions continued to be met. Additionally, the licensee recognized
that changes in plant ventilation equipment status created by refueling
outage activities could invalidate the assumptions of the analysis
supporting the compensatory action.
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The licensee initiated timely corrective actions to periodically l
reverify the initial conditions of the compensatory action. The i
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periodicity of the reverification varied based on the potential for the !
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condition to change. The inspector observed the reverification of the -
initial conditions following implementation of the licensee's corrective
actions.
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The inspector observed two other minor discreaancies during the review
of the compensatory action im)lementation. T1e control room door was
i not closed on March 24 when tie Unit 2 spent fuel pool bridge radiation i
monitor (2 EMF 4) alarmed although this appeared to be a condition for l
- closing the door. The inspector determined that the radiological
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a release (refer to Section 01.5). The inspector also found that the
accountability log sheet that specified individuals responsible for
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manually closing the control room door had not been signed for one day.
The inspector determined that the individuals involved were aware of
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The licensee documented the inspector's concerns in Problem
Investigation Process (PIP) Report 0-C97-0988 and initiated actions to
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determine: (1) if the response to the alarm was appropriate: (2) the
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cause of the administrative error: and (3) if a reverification process
- for compensatory actions is needed.
I c. Conclusions
The inspector concluded that control room operators were appropriately
l implementing their procedure for Loss of OAC when the OAC was
unavailable during the installation process. Additionally, operator
effectiveness in implementing a complex compensatory action was
challenged by numerous initial conditions and the lack of periodic
reverification to ensure that they were being continuously met.
01.4 Boron Dilution Mitiaation System Reliability
a. Insoection Scope (71707)
Du' ring the Unit 2 shutdown for refueling outage 2E0C8. multiple problems
, associated with the Boron Dilution Mitigation System (BDMS) were
encountered. The inspector investigated the nature of each problem and
reviewed the work history of the BDMS for both units. The inspector
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reviewed the FSAR and Technical Specifications (TS) and discussed system
performance and vulnerabilities with engineering personnel.
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b. Observations and Findinas
The BDMS consists of two trains and is designed to protect the reactor .
from an inadvertent criticality by automatically stopping the flow of i
unborated water to the core during shutdown conditions. Required by TS
in Modes 3, 4. 5. and 6. the BDMS uses two source range detectors to '
monitor the subcritical multiplication of the reactor core. An alarm ,
set)oint is continually calculated, and if the setpoint is exceeded,
eitler train of BDMS will automatically shut off both reactor makeup
water pumps, align the suction of the charging pumps to the Refueling
Water Storage Tank (FWST), and isolate flow to the charging pumps from .
the Volume Control Tank. Because these functions are automated, no
operator action is required.
Technical Specification 3.9.2 requires both trains of the BDMS to be
operable during Mode 6. If one or bcth trains are inoperable, the
licensee must either suspend core alterations or verify' that source +
range neutron flux monitors are operable with alarm setpoints
a)propriately calculated for the current (and, during core reload,
clanging) steady-state count rate. The licensee also must take
additional actions to verify that audible alarms are available in the
control room and containment, and that reactor makeup water pump flow
rates are within limits. In addition the BDMS is required operable
during Modes 3, 4 and 5 by TF 3.3.3.11.
kDuringtheUnit2refuelingoutage,multipleproblemswiththeBDMSwere
encountered. On March 25. Unit 2 BDMS interlock testing revealed a
failure to secure the reactor makeup water pumps. The failure was
attributed to a failed optical isolator. On March 28 during core
offload to the Spent Fuel Pool, a spike on the B train source range
instrument caused the charging pump suction to swap from the Volume
Control Tank to the FWST.' This spike was attributed to noise generated
by welding activities during the Operator Aid Computer replacement and
exacerbated by a loose plug at the data processing cabinet. A third
problem, which also occurred during the core offload, was associated
with a shutdown monitor that failed to a zero signal reading. Because
of the latter two problems the BDMS was declared inoperable, and the
required TS actions were performed.
Problems with the BDMS had been encountered periodically in the past.
According to the licensee's Work Management System (WMS), numerous work
requests have been written since 1987 for the BDMS. Since 1986. 134
work requests have been closed for the Unit 1 BDMS: since 1987. 83 work
requests have been closed for the Unit 2 BDMS. The inspector could not
consistently determine if specific work requesis were generated to
resolve system problems or if they were "onerated for other reasons
(e.g. nameplate installation). Nonetheles:.. the volume of work requests
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related to this system seemed high. The inspector expressed to the t
l licensee a concern with BDMS reliability and availability, as well as
the resulting impact (i.e., additional calibrations and monitoring) to
l control room operators. The licensee had come to the same conclusion *
through a system review independent of the NRC's inspection. Based on !
their findings, the licensee had recently decided to incorporate the !
BDMS into the site's Top Equipment Problem Resolution (TEPR) program. l
c. Conclusions
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Problems encountered with the BDMS during the' Unit 2 refueling outage
. were indicative of historical system performance problems, which affect ;
plant operation during modes 3. 4. 5 and 6. The inspector concluded I
that, since additional monitoring and calibration activities are
~ required when the BDMS is inoperable the BDMS has caused additional
control room operator workload to compensate for its unreliability. The
i- licensee has indicated that efforts are being initiated to improve
system reliability and, thereby. reduce operator burden through the TEPR
process. So that the licensee's efforts to correct this adverse system
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performance trend can be monitored to resolution, this issue is
identified as Inspector Followup Item 50-413.414/97-07-02: Boron
Dilution Mitigation System Reliability Resolution.
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01.5 Fuel Handlino Buildina Evacuation
a. Insoection Scooe (71707)
'The inspector evaluated the licensee's response to a radiation alarm
resulting in an evacuation of the fuel handling building that occurred
on March 24. The inspector reviewed licensee's procedures, conducted
interviews with involved personnel, and walked down the fuel handling
building.
b. Observations and Findinas
On March-24. the inspector responded to the control room when the ,
control room operators announced over the public address system the i
evacuation of the fuel handling building. During this time, the water
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level in the fuel transfer canal had been lowered to facilitate
maintenance on valve 2KF-122. Fuel Transfer Canal Isolation Valve. The
ins)ector found that the spent' fuel pool bridge radiation detector
(2EiF-4) had alarmed, and annunciator response procedure for alarm 2-
RAD-3 had been implemented. The control room o)erators conservatively
elected.to evacuate the fuel handling building )ecause the ah:r.m was not ;
expected.- The inspector verified that the control room operators i
- properly followed their procedures and that the appropriate level of I
supervisory oversight was maintained during the event. j
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The inspector also discussed the event with Radiation Protection '
personnel and found that proper actions were completed. Radiation
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Protection technicians surveyed the area and reported back to the ;
control room. Subsequently, the 2FME-4 alarm setpoint was raised to 2
three times the background radiation level in'accordance with approved !
procedures. Additionally, the inspector verified that the area survey :
map for the fuel handling building was updated, and the associated i
instrument log for 2 EMF-4 was changed to reflect-the new setpoint. !
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Because the alarm was not anticipated, the licensee initiated actions to i
evaluate the root cause of the event and determine appropriate l'
corrective action. Discussions with various plant )ersonnel revealed
that better coordination between affected plant wort groups and a !
possible procedure enhancement were needed during fuel transfer canal i
draining. This would provide for an increase in the alarm setpoint to i
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accommodate the expected increase in background radiation levels in the i
area with the canal drained.
! On March 25. the inspector performed a walkdown of the fuel handling !
building for area familiarization. During the walkdown the inspector '
performed a housekeeping assessment with emphasis on the licensee's
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adherence to foreign material exclusion (FME) requirements. ' The :
l inspector found that miscellaneous items (e.g. safety belt, tool bag, 2
face shield. grease gun, and paper) i.ere on the transfer canal catwalk :
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area and had not been logged into the cleanliness logbook. The licensee i
subsequently issued PIP 2-C97-08/1 to document this NRC observation and
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address corrective actions. '
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c. Conclusions
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The inspector concluded that actions by operations and RP personnel .in '
l response to the radiation alarm in the fuel handling building were good. "
! However, administrative controls over FME were not pro)erly im)1emented
t by personnel working near the fel transfer canal in t1e fuel landling
building.
01.6 Unit 1 Pressurizer Block Valve Control Circuit Failure
a. Insaection Scone (71707. 61726. 62707)
'
On March 20, Unit 1 pressurizer Power 0)erated Relief Valve (PORV) block
valve INC-33A failed.to. stroke closed w1en the valve control switch was
placed in the closed position during surveillance testing. A similar
failure of this valve had occurred on August 10, 1995. The inspector
reviewed the licensee's immediate actions to comply with TS action
requirements and an associated operability evaluation. The inspector
also reviewed PIP documentation (1-C97-0781 and 1-C95-1204) and the
licensee's evaluation of the potential repeat failure.
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- - Enclosure 2
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b. Observations and Findinos
The block valve is controlled with a three position control switch
(open/close/ override). During the surveillance test the valve failed to
close when the "close" Josition was selected. The licensee declared the -
valve inoperable and suasequently succeeded in closing the valve using
'
the " override" position. The inspector verified that the licensee met .
TS requirements after the valve was declared inoperable (TS 3.4.4.
Relief Valves).
Maintenance troubleshooting determined that the failure occurred in an
interlock portion of the block valve's control circuit. The interlock ;
uses position signals generated from stem mounted limit switches located ,
on the two other Unit 1 pressurizer PORV block valves. An operability l
evaluation performed after troubleshooting efforts concluded that the ;
block valve was operable since it would remain capable of closing as
required using the " override" position. The licensee's investigation of l
.
the previous failure in 1995 found that a limit switch lever shaft had
broken. The licensee has scheduled work orders to inspect the limit
switches and block valves during the next refueling outage and will
initiate further investigation if the same type of failure has occurred. J
. c. Conclusions '
A Unit 1 pressurizer PORV block valve control circuit failure occurred
which is a potential repeat of a previous 1995 failure. The licensee
.
I
has planned appropriate actions to determine the cause of the control '
circuit component failure when the components are accessible at the next
refueling outage.
08 Miscellaneous Operations Issues (92901. 92902)
08.1 (Closed) VIO 50-413.414/94-13-01: Failure To Follow Procedure NSD 703 4
And Station Directive 34.0.5 Requirements.
The inspectors reviewed the corrective actions identified by the
licensee for this violation in letters dated August 15. 1994, and August
8.1995, and verified that these actions were reasonable and complete.
The licensee's evaluation substantiated the violation and identified '
approximately 600 comaonents which were provided with an identification '
tag that identified t1e component number, but the tag did not include
the component's noun name as required by the site's procedures. The
inspectors performed a sample inspection of these components and !
verified that the identification tag included both the component number
and noun name. 4
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Enclosure 2
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08.2 (Closed) VIO 50-413/95-07-01: Inadequate Modification Procedure
Resulting in Loss of RHR.
TN/1/A/1331/00/01A. Procedure for the Implementation of NSM CN-11331.
Work Unit 01. did not receive adequate cross disciplinary review to
determine operational impact and scheduling to determine a safe plant
condition for implementation. The licensee's response dated April 28,
1995. stated that immediate actions were taken to revise the procedure
and stop work on modification implementation until all modification
packages were reviewed for similar errors. Additionally, the licensee
formed two self-assessment teams to determine root cause of the event.
The modification process was also revised to add new screening criteria I
for critical modifications that require an independent Senior Reactor 1
0)erator review to determine safe plant conditions for implementation of i
t1ese modifications. The inspector reviewed corrective action j
documentation (PIP 1-C95-0203) and verified that the licensee completed
these actions.
08.3 (Closed) VIO 50-413.414/95-07-02: Inadequate Valve Verification
Activities - Two Examples.
l
l Both examples of the violation involved personnel that failed to use
.
proper verification methods or independent verification of determining l
l
valve position or valve location. The licensee's response dated April l
! 28, 1995, stated that procedure revisions and additional training was l
provided for the plant staff that is involved in these verification
activities. The ins)ector verified that Operations Management Procedure
2-33. Valve and Breacer Position Verification and Valve Operations, was
revised to provide guidance for verifying the position of deenergized
motor operated valves. In addition, the licensee provided training to
, establish worker skills in error reduction. The inspector concluded
that the licensee's corrective actions were appropriate. j
1
l II. Mainwunce
M1 Conduct of Maintenance
1
1
M1.1 Unit 2 Outaae Maintenance Items
a. Insoection Scope (62707)
l The resident inspector monitored and inspected various work items during l
l the Unit 2 E0C8 refueling outage. Among these were: (1) a modification :
to replace the 2A and 2B Emergency Diesel Generator (DG) battery
chargers: (2) inspection and preventive maintenance on the 2B DG: (3)
the inspection and reconditioning of valves in the Safety Injection (NI)
system: (4) the repair of Loose Parts Monitoring System Channel 17.
Steam Generator (SG) manway: (5) the inspection of the containment sump
recirculation valve 2NI-185B: and (6) inspection of the A and D Reactor
! Coolant Pump (RCP) number 1 seals. The inspector discussed the
Enclosure 2
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12
maintenance activities with the licensee, obtained copies of the work
packages and observed portions of the maintenance in progress.
b, Observations and Findings
l'
(1) The Unit 2 125 Volt DC DG battery chargers were replaced under
station modification CN-21360. The inspector reviewed the work
Jackages associated with TN/2/A/1360/00/02E, which governed the A
Xi battery charger replacement., and TN/2/A/1360/00/03E, which
governed the B DG battery charger replacement. The inspector
verified that an 8-hour load test on DG chargers- 2A and 28 a
polarity check, output voltage check and current check were ,
successfully completed before the battery chargers were installed.
Steel frames and grout pads were fabricated for the chargers. The
inspector also verified that provisions for maintaining electrical i
separation, fabricating and installing electrical enclosures,
grounding cables, sealing the cable terminations, and using
crimping tools were included in the work packages. Cable
installation was ')rocedurally controlled, and electrical
isolations and ca]le terminations were recorded in the associated
procedure. A charger capacity test was satisfactorily performed,
the battery was equalized and charged, batteries were inspected.
. and the charger's high and low voltage relay alarms were
calibrated.
(2) The inspection and maintenance plan for the 2B DG included
activities typically performed on a five-year interval. The
l inspector observed portions of the activities in progress and
reviewed the work package and associated work orders, The
licensee disassembled sections of the DG: cleaned the engine
block; replaced hoses: refurbished the engine-driven fuel oil
pump: inspected cams and rollers: inspected the jacket cooling
water pump drive gear: inspected strainers for the starting air
system; and inspected and refurbished a temperature regulating
valve in the DG jacket cooling water system.
(3) Multiple check valves, suspected of leaking, were inspected during
l the outage. The licensee inspected valve 2NI-171, Safety
, Injection pumps to RCS loop C cold leg injection header check
valve, and determined that the valve had low seating contact. A
l minor modification was generated, and the disc was replaced with a
new disc of a different design that provided better seating
integrity.
Valve 2NI-175. RHR header A to RCS Loop C cold leg check valve,
was inspected: the valve was cycled, and the disc operated freely ,
without binding. The valve body and disc seats had no indication H
of degradation. The valve body and disc seats were cleaned, and a '
visual inspection revealed wide seat contact.
, Enclosure 2
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Valve 2NI-176 RHR Header A to RCS Looi D cold leg check valve.
showed no evidence of seat wear or leacage. The licensee cleaned
the seating surfaces and determined that they were finely. polished
.
'
with no indication of degradation.
l The disc in valve 2N!.-169. Safety Injection pumps to RCS lcop D
l cold leg injection header, was replaced, and the valve body seat
l was lapped until good contact could be visually verified. A-small
!
defect was polished out of the valve bonnet. The defect was i
believed to have caused minor external leakage in December 1995
and had been seal welded at that time to stop the leakage.
The inspector did not identify any concerns associated with the NI
system check valve maintenance.
(4) Unit 2 Loose Parts Monitoring System Channel 17. SG manway, was
repaired during a forced outage in December 1996. The channel had
been declared inoperable on January 2, 1996. Subsequent
troubleshooting revealed that the failure of the channel
,
' originated in the field. The licensee initiated a work request to
repair the channel during an outage window, at which time the
necessary containment entry could be made. To notify the NRC that
.
Channel 17 of the Loose Parts Monitoring System was inoperable for
.
longer that 30 days, the licensee submitted a s)ecial report on
l February 11, 1996, in accordance with Selected .icensee
Commitment Section 16.7-4, and TS 6.9.2.
The inspector discussed the repair with licensee personnel,
reviewed the associated work order. WO 96000758-01, and verified ,
that the channel )roblem had been corrected. The licensee had
determined that tie acoustic sensor' had an open _ connector at the- :
female hard line connector point. The sensor was replaced and-
!
satisfactorily tested. The channel was returned to service on
December 16, 1997.
(5) Prior to the last refueling outage-(2EOC7) the licensee determined
! that containment sump recirculation valves NI-184A and NI-185B.
l double-disc gate valves, were susceptible to pressure locking.
! During 2EOC7 the licensee im)lemented a station modification to
l ,
install a bonnet vent on eac1 sump recirculation valve. The >
1
bonnet vents provided a relief path from the valve body to the
residual heat removal (RHR) aump discharge line to preclude
pressurization in the valve Jody and subsequent wedging of the
i
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valve discs into their respective seats. The bonnet vent valves
were intended to remain open during full )ower o)erations,
although they could be. closed to isolate RHR leacage past the
7 containment-side valve disc.
I During startup from the- previous refueling outage. 2EOC7.- the
i
licensee determined that the containment-side seat of 2NI-185A was
.
Enclosure 2
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leaking. Since the bonnet vent valve (2NI-488) bypassed the RHR :
i suction-side disc a minor flow 3ath was created from the FWST. !
L via the RHR suction header. to t1e containment sump. To block the !
l leakage, vent valve 2NI-488 was locked closed. A work order was i
- generated to inspect and repair 2NI-185B during 2E0C8. ;
l The licensee opened the valve to inspect the seatirig surfaces l
during the refueling outage: the inspection results were
~
l
documented in PIP 2-C97-1066. At several locations around the '
perimeter of the containment-side valve body seat, small
l semicircular indicat ions were visible. The containment-side disc
l- seat had similar marks where the two surfaces had mated. The i
licensee could not determine why the pattern was present on the '
l valve body seat, nor coula the valve vendor explain these !
- indications. The indications in the seat surfaces were the likely !
! cause of the seat leakage during the previous operating cycle.
)
l
'
The licensee opted to leave the valve in its as found condition to !
avoid disturbing the seating of the RHR-side disc. The inspector i
,
'
questioned this decision, since they had been aware of the seat :
leakage during the preceding operating cycle and had ample time to ,
l plan for re) air during the refueling outage. The licensee !
l. explained tlat extensive time and resources could be allocated to i
l improve the containment-side di.;c seating, but that improvement
j. could not be guaranteed and that the RHR-side disc seating '
- integrity could be disturbed in the process. i
To test valve seating integrity.of the containment-side disc. the <
licensee applied 50 psig from the RHR pump side of the valve with
l vent valve 2NI-488 closed: no signs of leakage into the ,
'
containment sump were identified. Valve 2NI-488 was then' opened. !
! and leakage into the sump was observed. Valve DI-488 was then
- closed, and leakage into the sump was isolated oy the seating
l integrity of the RHR-side disc and the bonnet vent valve. An i
operability evaluation, documented in PIP 2-C97-1172. stated that
(1) valve 2NI-488 will be administratively controlled in the- l
closed position, and (2) valve 2NI-185A is operable with 2NI-488
, closed. The inspector concluded that the o)erability evaluation
i and actions taken to address seat leakage w1ile accounting for
! pressure locking and thermal binding were appropriate.
(6) The inspector observed RCP seal inspections and maintenance. The
! ins)ector also reviewed the task completian comments associated
wit 1 work orders 96098973-01 and 96098974-01 (for 2A and 2D RCP
seal work, respectively). The 2D RCP numoer 1 seal was cleaned
and inspected verified to be in good condition. and reinstalled.
, A chip was found in the outer edge of the 2A 'RCP number 1 seal
'
surface. A new set of stationary and running seals was installed,
j and the maintenance personnel verified that the seal moved freely
j up and down.
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Enclosure 2
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The inspector noted that RCP seal work was conducted in confined
areas around the RCPs. The work areas were difficult to access
and cramped. In addition, cleanliness and lighting levels during
the maintenance activities were adversely affected by the cramped
working spaces.
c. Conclusions
The inspector concluded that, in general, outage-related maintenance '
activities were ap]ropriately conducted. Although multiple barriers to
minimizing the risc of human error during RCP seal maintenance were
noted, the ins)ector was unaware of any human performance problems
associated wit 1 the work.
M1.2 Unit 2 Nuclear Service Water Pumo Motor Reolacement
a. Insoection Scope (62707)
The inspector reviewed the licensee's resolution to elevated vibration
levels associated with the 2B nuclear service water pump / motor assembly.
The 2B nuclear service water pump has experienced intermittent periods
of elevated vibration since 1994. During the inspection period, the
. licensee identified problems with the condition of the s
service water replacement motor stored in the warehouse.Accordingly,
pare nuclear
the inspector reviewed the results of previous licensee assessments of
spare motor storage practices, previous motor failures, and an ongoing
licensee assessment of maintenance and storage practices for spare
motors.
b. Observations and Findinas
The 28 Nuclear Service Water pump is a smooth running pump with normally
low measured vibration levels. In 1994 and 1995 the pump / motor assembly
3eriodically experienced an increase in vibration relative to its past
)aseline performance and also relative to the other nuclear service
water pumps. The relative increase in vibration levels caused the pump
to enter Alert levels although it continued to remain in the smooth
running range, As a result of this experience, the licensee performed
extensive inspection of this pump and motor during the current refueling
outage. Internal inspection of the pump showed no damage or
degradation. Vibration measurements made during an uncoupled run of the
motor indicated that the source of elevated vibrations was confined to
the motor. Based on additional analysis of vibration dr.ta performed by '
Electrical System Support (ESS) personnel, the licensee determined that
an internal rub was occurring in the motor and elected to replace it.
The spare nuclear service water pump motor developed severe oil leaks
'
from its lower bearing during initial check out runs performed in the
motor test shop prior to its installation. Inspections of the saare
motor internals performed by an offsite vendor determined that tie lower
Enclosure 2
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bearing surfaces were partially melted due to rubbing or inadequate
lubrication. Additional testing revealed more problems and the spare
motor was considered unacceptable for use and required extensive rework
and repair. The licensee subsequently performed internal inspections of l
the installed nuclear service water pump motor and determined the cause I
of the eleyated vibration resulted from mechanical looseness in the ,
upper bearing components. An off center condition in the lower bearing 1
housing was also discovered. The licensee corrected these '
adeficiencies, which eliminated the elevated vibration characteristic as i
measured in uncoupled runs and coupled inservice pump tests. l
In 1996, a residual heat removal pump motor failed soon after functional
testing. The licensee determined that poor storage conditions may have
contributed to this failure (refer to NRC Inspection Report 96-13). The
licensee has recently performed two assessments of motor storage and I
handling practices and identified several findings and recommendations. I
Inspector Followup Item (IFI) 50-413.414/97-07-03, Review Corrective
Actions For Storage and Handling Assessment Findings, is identified to
verify that the licensee has completed corrective actions resulting from
the followirig assessments: (1) Assessment Report CTS-09-96. Electric i
Motor P.M. - 12/2/96; and (2) Assessment Report SA-97-61(CN)(SRG), j
Assessment of Warehouse Material Condition - 4/23-28/97.
.
c. Conclusions
The licensee's resolution of long-standing elevated vibration levels ,
associated with the Unit 2B nuclear service water pump motor was very !
good. Deficiencies identified with a spare nuclear service water pump
motor, a previous motor failure, and findings identified by licensee
assessment of warehouse storage and handling 3ractices raised questions
about control and storage of spare motors. T1e issue is identified as
an Inspector Followup Item and will be reviewed during a future
inspection.
1
M2 Maintenance and Material Condition of Facilities and Equipment
M2.1 Observation of Unit 2 Inservice Insoection Work Activities
a. Insoection Scope (73753)
The present Unit 2 E0C8 refueling outage was the first outage, of the
first inspection period, of the second inservice inspection interval.
The applicable code for Unit 2, for the second inservice inspection
interval was the American Society of Mechanical Engineers (ASME) Code
l Section XI, 1989 Edition, no Addenda. The inspector reviewed
l documentation and observed ultrasonic, magnetic ) article, and liquid
l
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penetrant examination activities to determined w1 ether the inservice
inspection (ISI) activities were performed in accordance with Technical
specifications (TS), the applicable ASME Code, and/or requirements
imposed by NRC/ industry initiatives.
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Enclosure 2
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b. Observations and Findinos
The inspector reviewed the ISI outage examination plan and certification
records for all NDE examiners aerforming ISI examinations this outage.
l The following procedures, whic1 were used in the examination activities
observed by the inspector, were reviewed for technical content:
- NDE-600. " Ultrasonic Examination of Similar Metal Welds in Wrought l
Ferritic and Austenitic Piping." Revision 9
.
NDE-610. " Ultrasonic Examination of Dissimilar Metal Welds and
Cast Austenitic Welds Using Refracted Longitudinal and Shear i
Waves." Revision 4
.
NDE-660 " Ultrasonic Examination of Reactor Pressure Vessel Head
. NDE-25. " Magnetic Particle Examination." Revision 17
. NDE-35. " Liquid Penetrant Examination." Revision 16
Examinations of the following components were also observed by the
. inspector to determine if the examination procedures were followed,
whether examination personnel were knowledgeable of the examination
method and operation of the test equipment, and if the examination
results and evaluation of the results were recorded as specified in the
ISI program and NDE procedures.
. Welds Examined NDE Method Used
2RPV-101-101*** Ultrasonic Examination
2RPV-102-101*** Ultrasonic Examination
2CA-59-8 Ultrasonic Examination
2CA-59-11 Ultrasonic Examination
2RPV-101-101 Magnetic Particle Examination i
2CA-59-8 Magnetic Particle Examination i
2CA-59-11 Magnetic Particle Examination
2NV-242-3 Liquid Penetrant Examination
2NV-242-4 Liquid Penetrant Examination
2NV-242-10 Liquid Penetrant Examination 1
2NV-242-11 Liquid Penetrant Examination l
2RPV-W80-101SE Liquid Penetrant Examination i
2RPV-W81-101SE Liquid Penetrant Examination
2RPV-W82-101SE Liquid Penetrant Examination
2RPV-W79-101SE Liquid Penetrant Examination
2RPV-W80-101 Liquid Penetrant Examination
, 2RPV-W81-101 Liquid Penetrant Examination
l 2RPV-W82-101 Liquid Penetrant Examination
l 2RPV-W79-101 Liquid Penetrant Examination
!
! Enclosure 2
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- Note: Only portions of the 0 degree and 45 degree scans for these !
,
reactor vessel head welds were observed due to radiation dose >
limitations.
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c. Conclusion
NDE personnel certifications records, weld examinations, and NDE
examination procedures were in accordance with Code requirements.
M2.2 Observation of Unit 2 Steam Generator Eddy Current Data Acouisition
Activities
a. Insoection Scooe (73753)
The inspector reviewed documentation and observed eddy current data ,
l acquisition activities to dstermine whether these activities were i
performed in accordance with Technical Specifications (TS), the 1989 j
Edition of Section XI to the ASME Code, and requirements imposed by -
NRC/ industry initiatives. ,
b. Observations and Findinas
,
i
l. The licensee was performing bobbin coil eddy current examinations of 62% !
of the tubes in all four steam generators for Unit 2. In addition, a i
25% sample of the hot leg tube sheet transitions in each steam generator '
will be examined using a motor rotating pancake coil (MRPC). At the
time of this ins)ection the licensee had just started the examination
- activities and t1e data acquired was being sent directly to the McGuire
'
Nuclear Plant for analysis. Therefore, the inspector's examination of
l
'
these activities was limited to review of the outage eddy current
inspection plan, examiner and equipment certifications, and review of
l
examination procedures No. NDE-707 Revision 3, "Multifrequency Eddy
Current Examination of Non-Ferrous Tubing. Sleeves and Plugs Using a
Motorized Rotating Coil Probe", and No. NDE-701 Revision 3.
"Multifrequency Eddy Current Examination of Steam Generator Tubing at
McGuire. Catawba and Oconee Nuclear Stations and observation of the eddy
.
i
current data acquisition process,
l- c. Conclusion
Review of the eddy current outage plan, equipment setup and acquisition
procedures, personnel and equipment certifications, and observation of
l data acquisition activities revealed that required documentation was
l available and complete. and data acquisition personnel were
l knowledgeable of the eddy current examination process.
l
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Enclosure 2
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M2.3 Unit 2 Flow Accelerated Corrosion (FAC) Proaram l
a. Insoection Scooe (49001) !
l
The inspector held discussions with the licensee's erosion / corrosion !
engineers to determine the scope of FAC examinations scheduled for this
outage: the condition of the plant piping as revealed by inspection: the
extent of pipe replacement recuired: and whether proper examination
expansion was performed when cefective components were found.
b. Observations and Findinas
i
The licensee's FAC program for Unit 2 was based on the Electric Power
Research Institute's (EPRI) Document No. NSAC-202L. " Recommendation for
an Effective Flow Accelerated Corrosion Program." Revision 1. In ,
addition. EPRI's CHEC Works Computer Codes were used, as well as '
portions of the licensee's prev'ous program for erosion / corrosion to
identify components which will require examination. Initially, a sample
of 55 components were scheduled for ultrasonic examination during the
EOC-8 refueling outage. The sample also included the entire component.
upstream and downstream of the initial component. The licensee planned !
to replace six components without further examination, based on '
.
corrosion growth rates confirmed last outage. The examination of
components for FAC this outage were approximately 40% complete when
audited by the inspector. As a result of these examinations, five
additional components will be replaced this outage. The inspector
verified that expansion ins)ections.were correctly performed as a result
of the components found to 3e unacceptable based on inspections
performed this outage. The inspector also inquired as to why the
initial inspection sample was so small. The licensee stated that
smaller samples with a high volume of essential components. based on
tracking and trending was now possible on Unit 2 for the following
reasons:
. Significant previous replacements of components with
erosion / corrosion resistant materials.
. Changes in secondary chemistry control have reduced wear rates
significantly.
. The entire upstream and downstream components from a sample
'
selected for inspection are also examined.
. Unit 2 was designed with heater drains and moisturizer separator
reheater drains which have erosion / corrosion resistant materials
downstream of all control valves.
. FAC program maturity.
The inspector agreed with the licensee's reasoning.
, Enclosure 2
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c. Conclusion
,
The licensee has implemented an effective program for the detection of )
l
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flow accelerated corrosion in components. This program was based on '
recommendations found in recognized industry standards. !
M7 Quality Assurance In Maintenance Activities .
l M7.1 Maintenance Self Assessment Prooram
a. Insoection Scone (62707. 40500)
The inspector reviewed the status of maintenance and work control self-
assessment programs. The inspection included review of NSD 607. Self-
Assessments; maintenance and work control annual assessment plans for i
1996 and 1997: selected self-assessment reports; and maintenance / work l
control performance indicators,
b Observations and Findinas
The licensee's self-assessment program consisted of two types of self- l
assessments, routine and non-routine. Routine assessments were
'. performed on a quarterly or semi-annual basis and included topics such j
as PIPS, Job Observations. Rework. Material Condition / Housekeeping. Work
Order Quality. Budget. Radiation Dose / Contamination. Planning, and Work
Control Process. Non-routine assessments were performed when the need i
was apparent to management to assess a certain area or function. Some 1
examples were Procedure Use and Adherence. Environmental Compliance.
Pre-job Briefings. Control of Vendors, and Work Task Skills. Corrective
actions from the self-assessments were tracked for completion through
PIPS.
The inspector noted that the self-assessments that were reviewed !
effectively identified areas for improvement, and appropriate corrective '
actions were recommended and entered in the Problem Investigation '
Process for resolution. Of the routine assessments reviewed the
inspector considered the quarterly assessment of Job Observation Trends,
initiated in 1997, to be an effective use of the data generated by first
line supervisor observations.
Since the initiation of the Maintenance / Work Control Self-Assessment
Programs in mid and late 1995. performance indicators such as work order
backlog, schedule efficiency, and control board indication problems all
showed improving trends.
c. Conclusion ;
'
Based on the inspection described above. the inspector concluded that
the maintenance / work control self-assessment programs effectively
i
identified areas for improvement and appropriate corrective actions.
Enclosure 2 4
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The self-assessments apparently contributed to improvemert. in the
performance of the Maintenance and Work Control organizations.
III. Enaineering
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El Conduct of Engineering
El.1 Unit 2 Control Rod Tio Crackina
l
a. Insoection Scoce (61726. 37551)
During routine outage related examinations of Unit 2 control rod .
,
assemblies, the licensee identified a higher than expected number of
! control rods with tip cracking. The inspector reviewed the licensee's
L testing procedure, results of the examinations, and corrective actions
- _ for test failures,
b. Observations and Findinos
l Industry experience has shown that control rods develop tip cracking as
! a result of cladding interaction caused by swelling of the absorber
l
material inside this portion of the rods. . Tip cracking and other
.
potential control rod defects such as mechanical wearing are monitored
every refueling outage by the licensee using procedure PT/0/A/4150/26.
Rod Control Cluster Assembly (RCCA) Ultrasonic / Eddy Current Testing. ,
The inspector. discussed the results of the testing with reactor '
engineering personnel. The inspector observed that twenty.six control
rod assemblies were found with indications of tip cracking. This
-
exceeded the expected number of twelve control rod assemblies aredicted ,
to have tip cracks The licensee ordered additional rod assem) lies '
fabricated by the vendor and replaced each control rod assembly that had-
evidence of tip cracking. The inspector verified by reviewing control
rod assembly deficiency evaluations that the twenty six assemblies were
replaced. '
c. Conclusions
The licensee's actions to replace all control rod assemblies that had
evidence of tip cracking were appropriate.
E2 Engineering Support of Facilities and Equipment
E2.1 Review of Tentative Repair Activities for the Manway Cover on the Unit 2
Pressurizer
a. Insoection Scone (62001)
!
l The Catawba Unit 2 pressurizer manway cover experienced a leak during
i the end of cycle 8 shutdown for refueling. To repair the leak, the
- licensee elected to use an alternate method of repair consisting of a
1
- Enclosure 2
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welded diaphragm, in lieu of a flexitallic gasket. The licensee also
planned to replace the bolts and nuts on the manway cover with studs and
nuts. Another issue addressed in this modification was the inspection
- and clean-up of the boric acid which had leaked from the flange of the
!
manway behind the insulation on the pressurizer. The inspector
- reviewed this modification to ensure that documentation required for
!
this repair was available, and that inspection and cleanup of the boric ,
l acid crystals behind the pressurizer was properly addressed. 1
b. Observations and Findinas
'
In 1987, the licensee experienced several stuck bolts on the Unit 1
pressurizer manway. At that time the licensee used the alternate method
of repair delineated in the Westinghouse Technical Manual for the
pressurizer. This repair consisted of using a welded diaphragm, in lieu
of a flexitallic gasket. In addition, the licensee substituted studs
for the bolts used in the manway flange. At that time the licensee also
l realized that this same modification may some day be required for Unit
2. so 10 CFR 50.59 evaluations for the alternate modification method and
calculations for the stress analysis of the studs and nuts were !
conducted for each Unit in 1987. The inspector reviewed this I
documentation as well as the Westinghouse Pressurizer Technical Manual
. and drawings for this alternate method of repair. The information
reviewed was found to be satisfactory.
,
The inspector was initially concerned with the licensee's tentative I
plans to remove insulation only from the top and bottom of the
pressurizer in order to flush the boric acid crystals from behind the
insulation, and to use technical justification based on boric acid
corrosion rates documented in an EPRI document (TR-102748S) for
acceptance of any possible damage to the pressurizer. The inspector's
concern was based on the fact that the corrosion rates given in the EPRI
document differed significantly from the corrosion rates established by
Westinghouse under similar conditions and documented in NRC Generic
Letter 88-05 " Boric Acid Corrosion of Carbon Steel Reactor Pressure
Boundary Components in Pressurized Water Reactor Plants". In addition,
the inspector did not believe that the plan to use technical
justification met the intent of Catawba's Nuclear Site Directive 3.3.16.
which stated. "When there is evidence that boric acid has run under !
insulation remove enough insulation during the inspection 3rocess to l
assure all boric acid has been identified and evaluated. S1ould the
investigation reveal no damage to the contaminated components, the area l
is to be cleaned until free of visible borori crystals." During
discussions held with senior licensee management, the inspector was
informed that the plans for boric acid damage examination and flushing
, on the pressurizer which were identified to the inspector were very
' tentative and only one of many options being considered. The inspector '
l was also informed that a meeting on this issue was planned for following
i
week and the decisions reached in this meeting would be forwarded to the )
i inspector for review. l
Enclosure 2
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On April 9.1997, the inspector was informed of the licensee plans for
inspection and cleaning of boric acid on the pressurizer. These plans
would remove three additional sections of insulation and would allow
visual inspection to be performed in spot locations from the top to the
bottom of the pressurizer. The only disadvantage was visual inspection
could only be performed on the lower side of each of the sup) ort rings
except the top support ring. The licensee proposed that teclnical
l justification be used for the acceptance of the up)er portion of each
support ring using the EPRI criteria which Westinglouse agreed was
,
a)propriate for this corrosion wear application. These actions resolved
!
t1e inspector's concerns.
l The licensee )lanned to flush the pressurizer shell with hot water for
l four to five lours in an attempt to dissolve the crystals and remove
them from the carbon steel surface. To verify that the flushing process
was effective in removing the boron, the licensee planned to collect
water samples hourly at the base of the pressurizer and obtain data on
- boron concentrations, expecting the concentrations to decrease over
l time. The inspector questioned the confidence level of the validation
l
plan as a function of sampling frequency, and asked if an hourly sample
would provide sufficient data to verify that boron concentrations were
.
indeed decreasing over time. The licensee agreed that more frequent
sampling would yield a more robust conclusion and planned to sample the
i flushing water every half hour. The ins)ector reviewed the results of
l
the pressurizer flushing, documented in )IP 2-C97-0952. and concluded
that the flushing plan was effective in removing any dried boric acid
!
from the pressurizer shell.
c. Conclusions
The inspector concluded that documentation for the modification of the
Unit 2 pressurizer manway was satisfactory and engineering
considerations for modification, inspection, and cleaning of the
pressurizer shell were very good. Results of the boric acid cleanup
indicated that the plan had been effective.
E2.2 Desian Control
a. Ir;soection
r Scope (37550)
The inspector reviewed modifications being implemented during the Unit 2
outage. A)plicable regulatory requirements included Regulatory Guide
1.64 and AiSI N45.2.11-1974. Quality Assurance Requirements for the
Design of Nuclear Power Plants 10 CFR 50.59,10 CFR 50 Appendix B the
. licensee's Quality Assurance Topica'l Report (Duke-1-A), and associated
l
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24
design control implementing procedures. The following modifications
were reviewed:
. VN 8303H Replacement of Limitorque Motors on 2NI-54A. 2NI-65B. 1
. CN 21377 Modify Safety Injection (SI) Logic to Delete Low Stear )
Pressure Input 1
. CN 21375 Upgrade Allowable Temperature for Some Auxiliary Feed
Water (CA) Piping.
l
b. Observations and Findinas )
1
The specified post modification testing requirements on the above I
modifications adequately verified the design function of the modified l
equipment. Implementation of the SI signal deletion (CN 21377) resulted I
in damage to six process cards in the Solid State Protection System l
cabinet due to short circuits experienced during wiring terminations. l
The damaged cards were identified during post modification testing.
Appropriate actions were initiated to replace the damaged cards and ,
verify the integrity of the remaining installed cards. '
Replacement Motor Operated Valve Limitorcue motors (VN 8303H) were set '
up using the VOTES testing procedures anc implementing the applicable GL 89-10 requirements. The modification was required because tie original
size motors for the NI valves were not available. Cracks were found on
the motor shafts' key way of the installed motors. Post modification
verification was accomplished by Quality Control inspections for the CA
piping support modifications to upgrade the allowable piping temperature
(CN 21375).
The 50.59 evaluations for the modifications were adequate. A regulatory
issue was pending on the 50.59 evaluation for the CA piping upgrade (NRC
Inspection Report 50-413.414/96-03). The SI logic signal deletion
safety evaluation was documented in licensing amendments 158 and 150.
c. Conclusion
Regulatory design control requirements were appropriately implemented
for the Unit 2 outage modifications reviewed during this inspection.
E4 Engineering Staff Knowledge and Performance
E4.1 Identification and Correction of Eauioment Problems
- a. Insoection Stone (37550)
The inspector reviewed the licensee's actions related to the
identification and resolution of MOV limitorque motor shaft cracking.
Enclosure 2
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Applicable regulatory requirements included 10 CFR 50 Appendix B and the
licensee's Topical Quality Assurance Program.
b. Observations and Findinas
<
industry experience reports in 1995 and late 1996 noted examples of
<
motor shaft key way cracking in large high speed limitorque MOV motors.
The reports generally indicated the problem occurred in 3600 rpm motors
sized at 80 ft-lbs and larger. There were ten applications identified ,
at Catawba which included the four cold leg accumulator isolation valves )
and the NI-183 valves on each unit. The licensee implemented a motor
shaft inspection into the GL 89-10 program in 1996. No cracks were 1
identified on the Unit 1 valves inspected during the previous outage. '
There were cracks identified on three Unit 2 valves inspected during the
current outage. Replacement motors of the original sizes were
unavailable therefore a minor modification was implemented to change
the motor sizes. The original 175 ft-lb motor on 2NI-183B was replaced
with a 150 ft-lb motor from Cold Leg Accumulator valve 2NI-54. The
original 150 ft-lb motors on 2NI-54A. 2NI-65B and 2NI-76A were replaced
with 80 ft-lb. 80 ft-lb. and 100 ft-lb motors, respectively. Valve
motor torque switch settings and parameters were revised to meet the
recuirements of the GL 89-10 program and motor / valve application.
. Adcitionally, the associated motor control center overload heaters were
replaced on each valve to be consistent with the motor protection
requirements.
c. Conclusion 4
The identification and correction of MOV shaft key way cracking in Unit
2 safety injection system valves was a good example of engineering
identification and resolution of equipment problems. Industry operating
experience was appropriately incorporated into licensee activities and
effectively eliminated a potential safety-related equipment failure '
mechanism.
E8 Hiscellaneous Engineering Issues (92903)
E8.1 .(flosed) VIO 50-413.414/96-13-04: Inadequate Design Controls - Two
Examples
Example 1-Selection of Main Steam Isolation Valve (MSIV) Solenoid
Valves: This item identified a discrepancy where the nameplate design
rating of MSIV solenoid valves was less than the maximum design pressure
of the instrument air system. The ins)ector reviewed the licensee's
response dated November 6. 1996. The Jnit 1 solenoid valves were
replaced with aapropriate valves prior to identification of the
discrepancy. T1e valve manufacturer certified by letter that the
l
existing Unit 2 solenoid valves were acceptable until replacement at the
i
next refueling outage. The inspector verified that the Unit 2 solenoid
l valves were replaced with upgraded valves during this refueling outage
Enclosure 2
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(MW0s 96070278. 96070289. 96070280. 96070287) and testing of the
replacement solenoid valves was performed satisfactorily (PT
2/A/4200/09. Engineered Safety Feature Actuation Periodic Test).
Examole 2-Standby Shutdown System (SSS) Make-uo Pumn . Calculation - This
item identified calculation design input errors ' 'd to the system
conditions and pulsation damper which were useo 4
.wify the Net
Positive Suction Head (NPSH) for the SSS make-up pum). The licensee's
November 6. 1996, response to the violation stated tie design inputs for
the SSS make-up pum) sizing calculation and the damper design would be
evaluated and opera]ility for the Unit 1 and 2 pumps verified. The
inspector reviewed the licensee's completed corrective actions and
verified that the in)ut errors were resolved. Additionally, the actions
to assure pump opera]ility were completed.
E8.2 (Closed) DEV 50-413.414/92-01-03.: Breaker Coordination
This deviation was closed based on NRC Inspection Report 50-413.414/96-
19.
E8.3 (Closed) VIO 50-413.414/96-12-03: Inadequate Design Controls For
Ensuring Containment Crane Wall And Floor Drain Screens Implemented
. Design Requirements. l
This item identified containment crane wall penetrations and floor drain i
screens that did not implement design requirements developed to preclude ;
transport of debris to the Emergency Core Cooling System sum) screens. l
The licensee's October 29, 1996. violation response stated tlat the !
crane wall Jenetrations were filled with cualified foam to preclude any
flow throug1 them and modifications were ceveloped correct the screen
size of the floor drain screens. The inspector reviewed the licensee's j
completed corrective actions, including minor modifications (CNCE-8116. )
8139. 8186) and drawing revisions (CN-1070-5. rev. 14). The inspector
also performed a walkdown of the unit 2 containment building and
verified that the modifications were installed.
IV. Plant Support
R1 Radiological Protection and Chemistry Controls
R1.1 Tour of Ridioloaical Protected Areas
a. Insoection Scooe (83750. 71750)
The inspectors reviewed implementation of selected elements of the
licensee's radiation protection program as required by 10 Code of
Federal Regulations (CFR) Parts 20.1201. 1208, 1501. 1502. 1601, 1703.
i 1802. 1902, and 1904. The review included observation of radiological
protection activities, including personnel monitoring controls, control
Enclosure 2
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of ra'dioactive material, radiological postings, and radiation area /high
radiation area controls,
b. Observations and Findinas
During tours of the Auxiliary Building and radioactive waste !
storage /handhng facilities. the inspector reviewed survey data and '
performed selected independent radiation and contamination surveys of
radioactive material storage areas. Observations and survey results
determined-the licensee was effectively controlling and storing
radioactive material. '
i - -
i
. ~The inspector reviewed records for selected employees who had recently ;
!
worn respiratory protection equipment. The inspector verified that for - <
the records reviewed, each worker had successfully completed respiratory
l protection training, was medically qualified, and was fit-tested for the
l specific respirator type used in accordance with licensee procedural
! requirements. All respiratory protection equipment observed during
facility tours was being maintained in a satisfactory condition. The -
licensee had continued to implement engineering controls for respirator
reductions.
. During plant tours, the inspector observed that Extra High Radiation
,
Areas were locked as required by licensee procedures. The inspector
l also observed dosimetry controls for these areas were also established
E
in Radiation Work Permits (RWPs) as required by licensee procedures. t
The licensee's records indicated that the licensee was maintaining :
approximately 145,000 square feet (ft2 ) of floor space as a
P Radiologically Controlled Area (RCA). Records also showed that the
licensee maintained approximately 800-1000 ft2 (or less than 1 percent)
of the RCA as contaminated area during non-outage periods. During the-
current outage period, the licensee was maintaining approximately 1200
'
2
. ft as contaminated area.
t The inspectors reviewed Personnel Contamination Event (PCE) reports
prepared by the licensee to track, trend, determine root cause, and any
necessary followup action. Approximately 49 PCEs had occurred in 1997:
of which, approximately 38 PCEs had occurred during the current Unit 2
outage. The inspectors reviewed PCE log sheets for the past three years
and noted PCEs continued to trend downward. The licensee attributed
this reduction to several planned contamination control initiatives,
,
.uch as: increased followup with workers following contamination events:
!
reduction of contaminated areas: and reductions in radioactive waste.
During facility tours. the inspectors observed that survey
instrumentation and continuous air monitors observed in use within the
-
! RCA were operable and currently calibrated. The inspectors observed a
survey instrument (portable frisker) in the Unit 2 Reactor Containment
( Building which had not been source checked as required by licensee
Enclosure 2
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Procedure HP/0/B1003/22. Paragraph 4.9. The licensee conducted an
immediate investigation and located another frisker in the Unit 2
Reactor Containment Building which was available for use in the area !
that had not been source checked. The licensee removed both instruments
from the work area and performed a source check of the instruments to
verify operability. Both instruments source checked satisfactorily.
The licensee also initiated a Problem Investigation Process (PIP) report
to investigate the problem. The inspectors informed the licensee that ;
using survey instruments that had not been source checked was a
violation of licensee procedure and TS 6.8.1. Procedures and Programs.
However, based on the licensee's immediate corrective actions and the
safety significance of the circumstances. this licensee identified and
corrected violation is being treated as a Non-Cited Violation consistent ,
with Section VII.B.1 of the NRC Enforcement Policy. NCV 50-413.414/97-
07-04: Failure to Source Check Survey Instruments as Required by
Licensee Procedures.
The ins)ectors reviewed controls for entering the RCA and performing
work. T1ese controls included the use of RWPs to be reviewed and
understood by workers prior to entering the RCA. The inspectors
reviewed selected RWPs for adequacy of the radiation protection
requirements based on work scope, location, and conditions. For the
. RWPs reviewed, the inspectors noted that appropriate protective
clothing and dosimetry were required. During tours of the plant, the
inspectors observed the adherence of plant workers to the RWP
requirements. The inspectors also verified the licensee was effectively
,. managing controls for any declared pregnant women in regards to
embryo / fetus doses as required by 10 CFR 20.1208. The licensee was
, holding current personnel dosimetry accreditation from the National
- Voluntary Laboratory Accreditation Program (NVLAP) as required by 10 CFR
20.1501.
c. Conclusions
Based on observations and procedural reviews, the inspectors determined
the licensee was effectively maintaining controls for personnel
monitoring. respiratory protection, control of radioactive material,
radiological postings, and radiation area /high radiation area controls
as required by 10 CFR Part 20. One NCV was identified for failure to
source check survey instruments as required by licensee procedure.
R1.2 Occuoational Radiation Exoosure Control Proaram
l a. Insoection Scooe (83750)
The inspectors reviewed the licensee's implementation of 10 CFR
- ' 20.1101(b) which requires that the licensee shall use, to the extent
practicable, procedures and engineering controls based upon sound
radiation protection principles to achieve occupational doses and doses
,
Enclosure 2
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to members of the public that are As Low As Reasonably Achievable
(ALARA).
b. Observations and Findinas
The inspectors review of the licensee's ALARA program determined that
the licensee had established an annual exposure goal of approximately
286 person-rem, which included the Unit 2 outage goal of 132 person-rem
and Jart of a planned Unit 1 outage to begin late in 1997. At the time
of t1e inspection the licensee was tracking approximately 9 person-rem
below previous estimates. The licensee had continued to track and trend
outage exposures for purposes of future outage preplanning and it was
determined that exposures continue to trend downward based on ALARA
initiatives. Several ALARA initiatives reviewed during the inspection
that attributed to lower personnel exposures included: improved
scheduling to optimize the use of shielding and reduce worker congestion
in areas; replacement of stellite valve components with components made
from low to no stellite materials: a successful crudburst during the
Unit 2 shutdown which reduced Unit 2 dose rates by approximately 15
percent lower than previous Unit 2 outages; increased use of shielding:
and a improved method for workers to initiate ALARA suggestions.
. During tours of the facility the inspectors also observed Radiation
protection (RP) technicians controlling access to work areas to minimize
Personnel exposure and briefing workers in the work areas as
radiological conditions changed. The inspectors also observed personnel
beir.g briefed on ALARA considerations during specific briefings l
conducted to address RWP requirements.
c. Conclusions ,
l
Based on licensee planning efforts to reduce source term and the )
licensee's efforts to achieve established exposure goals which were
challenging, the inspectors determined the licensee was maintaining
programs for controlling exposures ALARA and continued to be effective
j in controlling overall collective dose.
R5 Staff Training and Qualification in Radiation Protection j
a. Insoection Scoce (83750 and 84750)
,
Training was reviewed to determine whether radiation protection
technicians had been instructed in radiation procedures to minimize ,
radiation exposures and control radioactive material as required by 10 '
CFR 19.12.
t
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b. Observations and Findinas
The inspectors reviewed training requirements for RP technicians and the 4
continuing training curriculum for the period of January 1,1996.
Enclosure 2
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through April 5, 1997, which included industry events and topics to
minimize radiation exposure. The inspectors also interviewed RP
personnel and observed work practices to determine the effectiveness of
continuing training. i
c. Conclusions
Based on the training activities reviewed, the inspectors determined
radiation protection technicians were receiving an appropriate level of l
training to perform routine work activities involving radiation and/or
radioactive material.
R7 Quality Assurance in Radiation Protection and Chemistry
a. Insoection Scooe (83750)
10 CFR 20.1101 requires that the licensee periodically review the RP
program content and implementation at least annually. Licensee periodic
reviews of the RP program were reviewed to determine the edequacy of l
identification and corrective actions. '
b. Observations and Findinas
.
By reviewing RP procedures, observing work, reviewing industry
documentation, and performing plant walkdowns to include surveillance of
work areas by supervisors and technicians during normal work coverage, i
the inspector determined that Quality Assurance audits and Self- l
Assessment efforts in the area of RP were accomplished. Documentation
of problems by licensee representatives was included in Quality
Assurance Audits and Self-Assessment Reports. Corrective actions were
included in the licensee's Problem Investigative Process and were being
completed in a timely manner.
During the inspection, the inspector reviewed the licensee's self-
assessment processes for evaluating an event in which unsuspected resin
was found in the 2B containment spray heat exchanger on April 10, 1997.
The resin was analyzed by gamma isotopic analysis and determined to be
mixed bed resin. The licensee began immediate followup actions to
determine the extent of a Jotential spread of resins into plant systems
that could be affected. T1e licensee formed a Failure Investigation
Process Team to determine the source of the resin and to develop a
recovery plan. The team was divided into key areas to identify the root
cause, evaluate sluicing operations and alignments that could affect the
potential spread of resin, identify potentially degraded ecuipment.
identify components that could be potentially impacted, anc develop a
,
'
cleanup plan. The licensee's investigation revealed that the probable
source of the resin was a potential tear in a screenwire used to contain
! mixed resin inside of an ion exchanger. The ion exchanger is used
i
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during spent fuel pool cleanup evolutions. The licensee determined that
only a small amount of resin was present in the containment spray
Enclosure 2
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l system, and cleanup actions were initiated to remove the resin that had l
1
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been identified. A total of approximately 200 - 250 milliliters of
resin was removed from the spent fuel pool purification and containment !
<
spray systems. The licensee initiated actions to clean out ion 6
l exchanger post filter housings whenever filters are changed to help i
l eliminate the potential for the small amounts of resin from entering l
l
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into the containment s] ray system. The licensee's engineering ;
evaluation concluded tlat there were no operability concerns resulting .
i from this event, and the inspector concluded that the licensee's review
l for operability was logical. The inspector determined that the licensee !
!
was aggressive in performing a root cause analysis of the resin event. !
l and the licensee's assessments of the event were good. i
!
c. Conclusions i
!
The inspector determined the licensee was performing Quality Assurance !
Audits and effectively assessing the radiation protection program as !
required by 10 CFR Part 20.1101. The inspector also determined the :
licensee was completing corrective actions in a timely manner.
l
F2 Status of Fire Protection Facilities and Equipment
'.
'
F2.1 00erability of Fire Protection Facilities and Ecuioment
f
a. Inspection Scoce (64704) i
i
'
The inspectors reviewed open corrective maintenance work orders on fire
protection components and operation's list of out-of-service fire
protection equipment to assess the licensee's performance for returning
degraded fire protection components to service. In addition, walkdown !
inspections were made to assess the material condition of the plant's l
fire protection systems, equipment, features and fire brigade equipment. t
b. Observations and Findinos !
Maintenance and Ooerability of Fire Protection Ecuioment and Comoonents
l
As of March 31, 1997, there were approximately 22 fire protection )
related work requests-in which the work had not been completed. Most of ' i'
these involved minor corrective maintenance work items and did not
!
affect the operability of the components. All of these work requests. i
except for work request item 910001140, were initiated in 1997 or late
- 1996. Item 910001140 involved repairs to the fire pump suction screens
!
which were to be corrected by minor modification CE-3197. This work had
been completed except for the proper reinstallation of the suction
screens. As of the date of this inspection, these screens had not been ,
i fully installed to the botsom of the screen frame. This resulted in an !
estimated area approximately 78x11 feet in size near the bottom of the
pump suction pit not being filtered.
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Two of the three fire pumps take suction from the fire protection
suction pit. This suction pit was provided with two suction screens
with 3/8-inch mesh installed to filter and prevent raw lake water trash
and debris from entering the suction pit for the pumps and clogging the
suction inlets for the two pumps. The third fire pump takes suction
from the suction pit for the low pressure service water pumps.
The fire pump suction screens were found degraded in late 1990 and
repairs were initiated in 1991. Following these repairs. the suction '
screens were not properly reinstalled. Reportedly, a lifting beam
device was misplaced during the modification process. Without the beam
device the filters could not be properly installed. The Catawba Fire
Protection OA Program has been incorporated into the Duke Topical Report
GA Program as OA Condition 3. The Topical Report. Section 17.3.1.6
states that Duke has established a corrective action process whereby all i
personnel are to assure conditions adverse to quality are promptly
identified, controlled, and corrected. Also. Topical Report Section
17.3.2.13 - Corrective Action. requires conditions adverse to quality to
be corrected The failure to correct the degraded filter screens for
the fire pumps in a timely manner is identified as Violation 50-
413.414/97-07-05. Following this inspection, the licensee notified the
inspectors that these screens were properly installed on May 14. 1997.
.
Otherwise, the inspectors concluded that there was no significant
maintenance backlog associated with fire protection components.
Also, as of March 31. 1997, there were 22 degraded or inoperable fire
protection components. Most of these items were related to the Unit 2
refueling outage which was in progress. For example several fire
barrier penetrations were open for movement of materials through open
floor hatches and the CO2 system for the 2A diesel generator was removed
from service due to maintenance work being performed on the diesel
engine. The remaining degraded features were either in nonsafety-
related areas or were minor discrepancies which did not affect the !
operability of the system or component. Four of these items had been l
degraded since late 1996. the remainder had been degraded since early i
1997 The inspectors verified that appropriate com)ensatory measures i
had been implemented for the degraded components, w1ere required. One I
degraded component required a continuous fire watch and three degraded '
components required an hourly fire watch patrol. The remaining degraded I
components were considered operable and did not require any compensatory
actions. l
'
The inspectors toured the plant and noted that the operable fire
- protection systems were well maintained and the material condition was
- very good.
l
Enclosure 2
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Fire Briaade Eauioment: !
The fire brigade turnout gear was stored in a fire brigade equipment
building adjacent to the Unit 2 Turbine Building. A sufficient number ,
of turnout gear, consisting of coats, Sants boots, helmets, etc., was !
provided to equip the fire brigade mem)ers expected to respond in the i
event of a fire or other emergency. The equipment was properly stored '
and well maintained.
c. Conclusions
The low number of open maintenance work orders and degraded fire
protection components, in conjunction with the good material condition
of the fire protection components and fire brigade equipment, indicated
that, in general, appropriate em)hasis had been placed on the
maintenance and operability of tie fire protection equipment and
components.
The work to repair the suction screens for two of the three fire pump's
suction piping had been o)en since 1991 and was not complete. The lack
of prompt resolution of t1e work was identified as a violation.
.
F2.2 Surveillance of Fire Protection Features and Eauioment
a. Insoection Scone (64704)
The inspectors reviewed the following completed surveillance and test
procedures:
-
IP/0/A/3350/13. Revision Change 0 Retype 5. EFA System Detector
Test Procedure, Data Gathering Panel 10. Completed January 20,
1997.
-
IP/0/A/3350/16. Revision Change 0 Retype 2. EFA System Detector
Test Procedure, Data Gathering Panel 13. Completed February 6.
1997.
-
PT/0/A/4400/01A, Revision Change 0 Retype 32. Exterior Fire
Protection Functional Capacity Test. Completed January 29, 1996.
-
PT/0/A/4400/01S, Revision Change 0 Retype 25. Exterior Fire
Protection System - Raw Water Yard (RY) Fire Protection Flow
(Underground) Periodic Test. Completed April 9.1996 and December
5, 1996.
The frecuency of selected surveillance test procedures were also
reviewec,
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b. Observations and Find 1nas
The completed fire protection surveillance tests reviewed by the
inspectors had been appropriately completed and met the. acceptance ;
criteria. The test procedures were well written and met the fire !
3rotection surveillance requirements of FSAR Chapter 16.9. Selected ;
_icensee Commitments (SLC). The surveillance procedures for the ;
capacity tests on the fire pumps required test data for multiple points j
on the pump curve to be obtained. This data provided good verification l
of the pump's performance.
During the review of Surveillance PT/0/A4400/01A. the inspectors noted l
that the October 1995 surveillance test indicated that the water flow
through the piping system would not deliver adequate fire flows This
test is conducted every three years and measures the flow of water ;
through various sections of piping to determine if the system will '
provide an adequate flow path from the fire pumps to the various i
sprinkler and hose stations located in the plant to meet the required l
design head 3ressure and volume requirements. Following the October
1995 test, t1e system was extensively flushed and retested in April i
1996. This test found that the system remained deficient. The flow
tests were performed by isolating the normal loop piping such that the
. flow tests were through a single pipe. The system would provide the
required design flow rates as long as the loop flow paths were
maintained in service. ;
The licensee developed a major pipe cleaning and flushing project
utilizing the " hydro-lase" process which was performed by station
personnel working under the supervision and coordination of a vendor
specialist. During the pipe cleaning activities several automatic
sprinkler systems and hose stations were required to be removed from
service. The licensee coordinated this work to require a minim;m number ;
of systems to be inoperable at any one time. Appropriate compensatory l
actions, consisting of a fire watch with backup fire suppression, were ;
provided as remedial actions while the required fire suppression systems '
were inoperable. Based on the review of the work activities and
interviews with the plant staff, the inspectors concluded that good
coordination and oversight of these activities were provided. Following
completion of the pipe cleaning activities the underground piping was
retested in December,1996 and was found to be capable of delivering the
required fire flow.
The surveillance requirements for the fire protection systems were
contained in FSAR Chapter 16.9. The results of the inspector's review
I of these features is located in Section F3.
l
c. Conclusions
l
Good surveillance and test procedures were provided for the fire
protection systems and features. Procedure implementation was
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effective. The coordination of the fire protection water piping
cleaning project was excellent.
F3 Fire Protection Procedures and Documentation
a. Insoection Scooe (64704)
The inspectors reviewed the following procedures for compliance with the
NRC requirements and guidelines:
-
Nuclear Station Directive 112. Revision 0. Fire Brigade
Organization. Training and Responsibilities
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Site Directive 2.12.5, Revision 3. Control of Combustible
Materials Within the Protected Area
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Site Directive 2.12.6. Revision 3. Fire Protection. Detection and
Barrier Impairment Reporting
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Site Directive 2.12.7. Revision 4. Fire Protection / Detection !
! Remedial Actions
!.
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Site Directive 3.3.9. Revision 1. Hot Work Authorization
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FSAR Chapter 16.9. (Revision dated 1/30/96). Auxiliary Systems
(Fire Protection Systems)
-
Prefire Plans. Revision 6. Catawba Prefire Plans 6.1d Procedures
Plant tours were also performed to assess procedure compliance.
b. Observations and Findinas
The above procedures were the principle procedures issued to implement
the facility's fire protection program. These procedures contained the
requirements for program administration. controls over combustibles and
i ignition sources, fire brigade organization and training, and
o)erability requirements for the fire protection systems and features.
,
T1e procedures were well written and met the licensee's commitments to
!
the NRC.
The inspectors performed plant tours a"d noted that, even though the l
plant was in a refueling outage, implementation of the site's fire !
l prevention program for the control of ignition sources, transient ;
l combustibles, and general housekeeping was good. The accumulation of j
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transient combustible materials and the number of maintenance activities '
in process due to the refueling outage were-more than anticipated during
normal plant operations. However, appropriate fire prevention controls
were being applied to these activities.
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FSAR Chapter 16.9. Selected Licensee Commitments. Auxiliary Systems
(Fire Protection Systems) provides the operability and surveillance
requirements for the fire protection systems and components. The
inspectors compared these requirements to the requirements which were
formerly in the TS. These requirements remained essentially the same,
except for the following testing frequency changes: fire detectors.
from monthly to annually; fire protection valve alignments, from monthly
- to quarterly; and hose station inspection, from monthly to quarterly.
The licensee had recently changed these surveillance inspection
,
frequencies based on satisfactory results from performance based
l evaluat wis of these systems. The inspectors verified that appropriate ,
l 10 CFR 50.59 safety evaluations had been performed for these revisions. l
The trending data on the performance based surveillance inspections were !
reviewed and indicated that the reliability of these systems was greater l
than 99 percent. This substantiated the changes made to the !
surveillance frequency requirements. The operability requirements in
the SLC were adequate. However, the water supply and fire detection
systems were the only systems which had time limits established for
restoring inoperable components to operable status. This issue is being
evaluated further by the NRC and is identified as an Inspector Followup
Item pending completion of this review. IFI 50-413.414/97-07-06: Time
Limits for Restoration of Inoperable Fire Protection Components.
.
The prefire plans reviewed by the inspectors were found to be
satisfactory. A minor modification was in process to relocate and
remove some of the fire extinguishers presently installed within the .
plant. Also, a standard fire protection water supply system was I
scheduled to be installed by late 1991 for the nuclear service water '
intake pumping structure. The prefire plans were scheduled to be
revised upon completion of these modifications. In the interim.
controlled copies of the prefire plans had been marked to indicate the
plant changes as they were completed for each plant area.
c. Conclusions
The fire protection program implementing procedures were good and met
licensee and NRC requirements. Implementation of procedures for the
control of ignition sources, transient combustibles, and general
housekeeping was good. An issue regarding time limits for restoration
of inoperable fire protection components will be reviewed further by the
NRC.
F5 Fire Protection Staff Training and Qualification
a. Inspection Scope (64704)
The inspectors reviewed the fire brigade organization and training
program for compliance with the NRC guidelines and requirements.
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l b. Observations and Findinas
[ :
j The organization and training requirements for the 31 ant fire brigade
were established by Nuclear Station Directive 112. Revision 0. Fire i
Brigade Organization. Training and Res]onsibilities. The fire brigade I
for each shift was composed of a fire arigade leader and at least four
j brigade members from operations and approximately five members from
maintenance. The fire brigade leeder was a senior reactor o]erator i
(SRO) and was normally one of the unit shift supervisors. T1e other
members from Operations were non-licensed plant operators. One of the i
! fire brigade members was normally assigned the duties of fire brigade
safety officer to provide technical and administrative assistance to the
fire brigade leader and to hel) cssure the safe performance of each fire
l brigade member by checking eac1 member for appropriate dress out prior
l to entering the fire area, maintaining records of each fire brigade ,
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exposure to fire or radiatinn hazards, use of self contained breathing l
apparatus, and reviewing the prefire plans during the emergency for '
assurance that appropriate measures are being followed for compliance
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with applicable safety and fire hazards in the area. Assignment of a
l fire brigade safety officer was identified as a program strength.
l
Each fire brigade member was required to receive initial, quarterly and
.
annual fire fighting related training and to satisfactorily complete an
annual medical evaluation and certification for participation in fire
brigade fire fighting activities. In addition each member was required
i to participate in at least two drills per year.
.
As of the date of this inspection, there were a total of 34 operations
trained fire brigade leaders and 73 operations personnel and 29
maintenance personnel on the plant's fire brigade. Approximately 6 fire
brigade leaders.12 operations fire brigade members and 5 mintenance
fire brigade members were assigned to each of the five operations crews.
This was a sufficient number of personnel to meet the facilities fire
brigade procedure requirements for one team leader and nine members per
l shift.
The inspectors reviewed the training and medical records for the fire
brigade members and verified that the training and medical records were I
up to date. The facility utilized off-site qualified state certified
fire brigade training instructors and a state fire training facility to
perform the annual fire brigade training and practical fire training
,
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scenarios.
During this inspection, the inspectors witnessed a fire brigade drill
involving a simulated fire in an electrical motor for a component
cooling pump located on the 560 foot elevation of the auxiliary
building. The response of the fire brigade to the simulated fire was
- excellent. The brigade leader's direction and fire brigade members'
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performance, especially the safety officer, were outstanding. A
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critique to discuss the brigade performance and future enhancements was
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, held following the drill.
c. Conclusions
The fire brigade organization and training met the requirements of the
site procedures. Performance by the fire brigade during a drill was
excellent. The use of the fire brigade safety officer position during
fire emergencies was identified as a program strength.
F6 Fire Protection Organization and Administration
i
a. Insoection Scooe (64704)
]
The licensee's managemerit and administration of the facilities fire l
protection program were reviewed for compliance with the commitments to
the NRC and to current guidelines. )
b. Observations and Findinas
The Civil. Electrical. Reactor. Nuclear Engineering Manager was assigned
the responsibility for implementing the facility's fire protection
,. program. An engineer was assigned the task of coordinating the entire
fire 3rotection program and for coordinating the maintenance,
opera)ility and modifications on the fire suppression systems, fire
barriers, and fire barrier penetrations. Another engineer was i
responsible for coordinating the maintenance, o)erability and !
modifications on the fire detection systems. T1e Manager of Safety l
Assurance was responsible for providing appropriate training for the i
facility fire brigade and for providing guidance and support in the '
implementation of the facility's fire protection program. Support on
generic fire 3rotection issues was provided to the site by an engineer
assigned to t7e Corporate Nuclear Engineering Division.
A corporate Fire Protection Business Excellence Steering Team (BEST).
composed of representatives from each of the three Duke nuclear plants
and the corporate staff, was meeting monthly to discuss fire protection
issues and im)rovements needed to enhance the fire protection program at
each site. T1e inspectors reviewed the minutes for the first three
meetings in 1997 and noted a number of issues were under consideration
which, if im)lemented should improve the overall fire protection
program at t1e Duke facilities. The inspector concluded that these
meetings were a positive element of the facility's fire protection
program.
c. Conclusions
-
Strong coordination and oversight were provided over the facility's fire
protection program. The Fire Protection BEST was a positive factor in
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the identification of potential problems and in the development and
implementation of enhancements to the fire protection program.
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F7 Quality Assurance in Fire Protection Activities
!
l a. Insoection Scooe (64704)
The following audit report was reviewed:
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Audit SA-95-24(CN)(RA). Triennial Fire Protection Audit conducted
May 15 through June 8, 1995
b. Observations and Findinas
Audit SA-95-24(CN)(RA) was a triennial 0A audit of the facilities' fire
protection program. The licensee informed the inspectors that this was
the only comprehensive audit of the fire protection program performed
since Duke's December 18, 1991, request to use performance based
criteria for establishing auoit frequencies was approved by the NRC.'s
letter dated May 7. 1992. Previously, the TS had required annual,
biannual and triennial audits of the fire protection program. However,
based on the licensee's assessment of good fire protection performance.
. only this one triennial audit had been performed at Catawba in recent
years.
TS 6.5.2.9 identified a number of site audits which were performed under
the cognizance of the Nuclear Safety Review Board. The licensee's
December 18, 1991, letter indicated that the audit frequency for all of
these audits were deleted from the TS. and the OA Topical report was to
be revised to indicate that the " audits of selected aspects of
operational phase activities are performed with a frequency commensurate
with safety significance and in such a manner as to assure that an audit
of all safety related functions is completed within a period of two
years." The OA topical report was revised, but only requires an audit
of all "0A Condition 1 functions" to be completed within a period of two
years. Many of the audit items listed by TS Section 6.5.2.9 are
classified as OA Condition 2 or 3 functions. The specified time for
these audits are not listed in the OA topical report. The inconsistency
of not providing a specified frequency for Condition 2 and 3 functions
is being further reviewed by the NRC and is identified as Inspector
Follow-up Item pending completion of this review. 50-413.414/97-07-07:
Audit Frequency Requirements for Activities other than OA Condition 1
Functions.
The inspectors reviewed the audit findings from the 1995 OA report and
the corrective actions taken on the identified discrepancies. The
report indicated that a comprehensive audit had been performed with nine
findings identified. The corrective action on each finding had been
completed in a timely manner.
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c. Conclusions
The 1995 audit and assessment of the facility's fire protection program
was comprehensive and appropriate corrective action was promptly taken
to resolve identified issues. An issue regarding the control of 0A
audit frequencies will be reviewed further by the NRC.
F8 MiscellaneousFireProtectjonIssues
F8.1 Fire Protection Related NRC Information Notices
The inspector reviewed the licensee's evaluation for the following NRC 1
Information Notices (IN): '
-
IN 92-18. Potential loss of Shutdown Capacity During a Control
Room Fire
-
IN 92-28. Inadequate Fire Suppression System Testing
-
IN 93-41. One Hour Fire Endurance Tests Results For Thermal
Ceramics. 3M Company FS 195'and 3M Company E-50 Interam Fire ,
Barrier Systems I
..
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IN 94-28. Potential Problems with Fire Barrier Penetration Seals
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IN 9--31. Potential Failure of WILCO. LEXAN-Type HN-4-L. Fire Hose
Nozzles
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IN 94-58. Reactor Coolant Pump Lube Oil Fire
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The licensee's evaluations and corrective actions for these ins were
appropriate, except the evaluation documentation for some of the ins did
not fully indicate the results of the evaluations which were actually
performed.
V. Manaaement Meetinos
X1 Exit Meeting Summary
The inspectors ) resented the inspection results to members of licensee
- management at t1e conclusion of the inspection on April 30. 1997. On May 14
- a teleconference was held between Region II DRS management and licensee
management representatives to discuss the violation included with this report.
l The licensee acknowledged the findings presented. No proprietary information
t
was identified. .
Enclosure 2
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PARTIAL LIST OF PERSONS CONTACTED
Licensee
Bhatnager, A., Operations Superintendent
Birch. M., Safety Assurance Manager .
Christopher. S. , Emergency Planning Supervisor '
l Copp. S Nuclear Regulatory Affairs Manager
'
Coy. S., Radiation Protection Manager i
Forbes. J., Engineering Manager '
Giles, R. Work Control Inservice Inspection Coordination ,
Harrall. T. Instrument and Electrical Maintenance Superintendent '
- Kelly. C.. Maintenance Manager
! Kimball. D., Safety Review Group Manager
! Kitlan. M., Regulatory Compliance Manager '
Kulla D. Civil Engineering Supervisor
McCollum W., Catawba Site Vice-President
Nicholson. K., Compliance Specialist
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l Peterson. G., Station Manager
l. Propst. R., Chemistry Manager
Purser, M.. Senior Engineer
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l Robinson G., Work Control Execution Support
l Rogers D., Mechanical Maintenance Manager i
Tower, D., Compliance Engineer '
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INSPECTION PROCEDURES USED
IP 37550: Engineering
IP 37551: Onsite Engineering
IP 40500: Effectiveness of Licensee Controls in Identifying, Resolving, and
Preventing Problems
'
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IP 49001: Inspection of Erosion / Corrosion Monitoring Programs
IP 61726: Surveillance Observation
IP 62001: Boric Acid Program Prevention Program
IP 62707: Maintenance Observation
,
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IP 64704: Fire Protection Program
IP 71707: Plant Operations
l IP 71750: Plant Support Activities
'
IP 73753: Inservice Inspection
IP 83750: Occupational Radiation Exposure
l IP 84750: Radioactive Waste Treatment and Effluent and Environmental
Monitoring
IP 92901: Followup - Operations
IP 92902: Followup - Maintenance
IP 92903: Followup - Engineering
ITEMS OPENED, CLOSED, AND DISCUSSED
.
Opened
50-414/97-07-01 VIO OPEN Inadequate Procedure Resulting in
Loss of Spent Fuel Pool Cooling with
Core Off-loaded. (Section 01.1)
50-413,414/97-0? 32 1FI OPEN Boron Dilution Mitigation System
Reliability Resolution. (Section
01.4)
50-413.414/97-07-03 IFI OPEN Review Corrective Actions For
Storage and Handling Assessment
Findings. (Section M1.2)
50-413,414/97-07-04 NCV OPEN Failure to Source Check Survey
Instruments as required by licensee
procedure. (Section R1.1)
50-413.414/97-07-05 VIO OPEN Failure to Repair Degraded Suction
Screen Filters for Fire Pumps in a
Timely Manner. (Section F2.1)
50-413,414/97-07-06 IFI OPEN Time Limits for Restoration of
,
Inoperable Fire Protection
Components. (Section F.3)
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50-413.414/97-07-07 IFI OPEN Audit Frequency Requirements for
Activities other than OA Condition 1
Functions. (Section F.7) :
Closed
50-413.414/94-13-01 VIO CLOSED Failure to follow Procedure NSD 703
and Station Directive 34.0.5
requirements. (Section 08.1)
l 50-413/95-07-01 VIO CLOSED Inadequate Modification Procedure !
Resulting in Loss of RHR. (Section ,
i
08.2)
50-413.414/95-07-02 VIO CLOSED Inadequate Valve Verification
Activities - Two Examples. (Section
08.3)
50-413.414/96-13-04 VIO CLOSED Inadequate Design Controls (MSIV
Solenoid Valves). Standby Shutdown
System Makeup Pump Sizing
Calculation (Section E8.1)
.
50-413.414/92-01-06 DEV CLOSED Breaker Coordination (Section E8.2)
50-413.414/96-12-03 VIO CLOSED Inadequate Design Controls For
Ensuring Containment Crane Wall and
Floor Drain Screens Implemented
Design Requirements (Section E8.3)
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l
l LIST OF ACRONYMS USED
l
ALARA - As Low As Reasonably Achievable
ANSI -
American Nuclear Standards Institute
ASME - American Society of Mechanical Engineers
,
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BDMS - Boron Dilution Mitigation System
CA -
Auxiliary Feedwater (system)
CHEC - Designation for EPRI computer code
CFR -
Code of Federal Regulations
DEV -
Deviation
DG -
Diesel Generator
DPC -
Duke Power Company
EFA -
Fire Detection System
EPRI -
Electric Power Research Institute
ESS -
Electric System Support
FAC -
FME -
FSAR - Final Safety Analysis Report
FWST - Refueling Water Storage Tank
2
ft -
Square Feet
ft-lb - foot-pounds (force)
GL -
Generic Letter
. IFI -
Inspector Followup Item
IN -
Information Notice
IR -
Inspection Report
ISI -
Inservice Inspection
MOV -
Motor Operated Valve
MSIV - Main Steam Isolation Valve
NCV -
Non Cited Violation
NDE -
NI -
Nuclear Safety Injection (system)
NSD -
Nuclear System Directive
NSM -
Nuclear Station Modification
NRC -
Nuclear Regulatory Commission
OAC -
Operator Aid Computer
PCE -
Personnel Contamination Event
PIP -
Problem Investigation Process
PORV - Power Operated Relief Valve
psig - Pounds Per Square Inch Gauge
QA -
Quality Assurance
RCA -
Radiologically Controlled. Area
RCP -
Reactor Coolant Pump
RCS -
RHR -
RP -
Radiation Protection
rpm -
revolutions per minute
RWP -
Radiation Work Permits
SG -
SI -
Safety Injection
l SLC -
Select Licensee Commitments
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SSS -
Standby Shutdown System
TEPR - Top Equipment Problem Resolution
TS -
Technical Specifications
UFSAR - Updated Final Safety Analysis Report
VIO -
Violation
VN -
Variation Notice
WO -
Work Order
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