ML19263B940: Difference between revisions

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                                               $4lA
                                               $4lA AAKANSAS POWER & LIGHT COMPANY PCST OFFICE BOX 551 UTTLE ROCK. ARKANSAS 72203 (501) 371-.1000 January 12, 1979 1-019-5 Mr. Norman M. Haller, Director Office of Management Information and Program Control                                                        ,
      ,
AAKANSAS POWER & LIGHT COMPANY PCST OFFICE BOX 551 UTTLE ROCK. ARKANSAS 72203 (501) 371-.1000
  ,
January 12, 1979
,
1-019-5 Mr. Norman M. Haller, Director Office of Management Information and Program Control                                                        ,
                                                                                                  -
U. S. Nuclear Regulatory Commission Washington , D. C.      20555
U. S. Nuclear Regulatory Commission Washington , D. C.      20555


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Attached find the Monthly Operating Report for December 1978 for Arkansas Nuclear One - Unit 1.
Attached find the Monthly Operating Report for December 1978 for Arkansas Nuclear One - Unit 1.
This report includes an adjustment of 12MWH in the year-to-date and cumulative totals for both the gross and et electrical energy generated to correct recently discovered errors, very truly yours,          .
This report includes an adjustment of 12MWH in the year-to-date and cumulative totals for both the gross and et electrical energy generated to correct recently discovered errors, very truly yours,          .
                                                       ,  Y          l .1 *b Daniel H. Williams Manager, Licensing DHW:REI:tw Attachments cc: Mr. K. V. Seyfrit, . Director Office of ' Inspection & Enforcement U. S. Nuclear Regulatory Commission Region IV 611 Ryan Plaza Drive, Suite 1000 Arlington, Texas      76011
                                                       ,  Y          l .1 *b Daniel H. Williams Manager, Licensing DHW:REI:tw Attachments cc: Mr. K. V. Seyfrit, . Director Office of ' Inspection & Enforcement U. S. Nuclear Regulatory Commission Region IV 611 Ryan Plaza Drive, Suite 1000 Arlington, Texas      76011 Mr. John G. Davis, Acting Director [                                        D Office of Inspection a. Enforcement                                      ,
                                                                                            !
Mr. John G. Davis, Acting Director [                                        D Office of Inspection a. Enforcement                                      ,
a Washington, D. C.        20555                                              /
a Washington, D. C.        20555                                              /
                                                                                    -
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7 9 012 5 01Gi                  oevee_cc<, scu,- ur,ar ,, so,,,
7 9 012 5 01Gi                  oevee_cc<, scu,- ur,ar ,, so,,,
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                                                  .
.. . . -                                                  .
NRC M0tiTHLY OPERATIriG REPORT OPERATING'SUMt'ARY - DECEMBER,1978 9
NRC M0tiTHLY OPERATIriG REPORT OPERATING'SUMt'ARY - DECEMBER,1978 9
t UNIT 1 The unit. operated at approximately 100% reactor pcwer until 12/20, at 0200 hours, when a Main Feedwater Pump Vent valve bonnet blew off re-    -
t UNIT 1 The unit. operated at approximately 100% reactor pcwer until 12/20, at 0200 hours, when a Main Feedwater Pump Vent valve bonnet blew off re-    -
                                                                                    ,
sulting in an unisolatable steam leak. The unit load was reduced to 40% power to remove the pump from service for repairs. At 1045, af ter the unit was stabilized at 37% reactor power, a main turbine governor valve LVDT failed causing a loss o/ valve position control signal.
sulting in an unisolatable steam leak. The unit load was reduced to 40% power to remove the pump from service for repairs. At 1045, af ter the unit was stabilized at 37% reactor power, a main turbine governor valve LVDT failed causing a loss o/ valve position control signal.
The resulting incorrect signal caused the turbine electro-hydraulic control system to move the associated governor valve 100% open and re-duced steam line pressure sufficiently to trip the Steam Line Break Instrumentation and Control System (SLBIC), which tripped the turbine          .
The resulting incorrect signal caused the turbine electro-hydraulic control system to move the associated governor valve 100% open and re-duced steam line pressure sufficiently to trip the Steam Line Break Instrumentation and Control System (SLBIC), which tripped the turbine          .
and the. reactor. The. unit was placed back on line 12.9 hours later.
and the. reactor. The. unit was placed back on line 12.9 hours later.
                                                                                *    -
                                                                                ,
The Unit operated at approximately 90% reactor power until 12/31, when at 850 the main turbine developed a high vibration, The uni t was man-ually tripped. Initial investigation revealed damage to the L-2 row of blading. Unit shutdown continued throughout the remainder of the re-port period.
The Unit operated at approximately 90% reactor power until 12/31, when at 850 the main turbine developed a high vibration, The uni t was man-ually tripped. Initial investigation revealed damage to the L-2 row of blading. Unit shutdown continued throughout the remainder of the re-port period.
                                '.                                          -
                             ".}}
                             ".}}

Latest revision as of 20:50, 1 February 2020

Forwards Monthly Operating Rept for Dec 1978
ML19263B940
Person / Time
Site: Arkansas Nuclear Entergy icon.png
Issue date: 01/12/1979
From: David Williams
ARKANSAS POWER & LIGHT CO.
To: Haller N
NRC OFFICE OF MANAGEMENT AND PROGRAM ANALYSIS (MPA)
Shared Package
ML19263B941 List:
References
1-019-5, 1-19-5, NUDOCS 7901250164
Download: ML19263B940 (1)


Text

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$4lA AAKANSAS POWER & LIGHT COMPANY PCST OFFICE BOX 551 UTTLE ROCK. ARKANSAS 72203 (501) 371-.1000 January 12, 1979 1-019-5 Mr. Norman M. Haller, Director Office of Management Information and Program Control ,

U. S. Nuclear Regulatory Commission Washington , D. C. 20555

Subject:

Arkansas Nuclear One-Unit 1 Docket No. 50-313 License No. DPR-51 Monthly Operating Report (File: 0520.1)

Gentlemen:

Attached find the Monthly Operating Report for December 1978 for Arkansas Nuclear One - Unit 1.

This report includes an adjustment of 12MWH in the year-to-date and cumulative totals for both the gross and et electrical energy generated to correct recently discovered errors, very truly yours, .

, Y l .1 *b Daniel H. Williams Manager, Licensing DHW:REI:tw Attachments cc: Mr. K. V. Seyfrit, . Director Office of ' Inspection & Enforcement U. S. Nuclear Regulatory Commission Region IV 611 Ryan Plaza Drive, Suite 1000 Arlington, Texas 76011 Mr. John G. Davis, Acting Director [ D Office of Inspection a. Enforcement ,

a Washington, D. C. 20555 /

((

7 9 012 5 01Gi oevee_cc<, scu,- ur,ar ,, so,,,

[

NRC M0tiTHLY OPERATIriG REPORT OPERATING'SUMt'ARY - DECEMBER,1978 9

t UNIT 1 The unit. operated at approximately 100% reactor pcwer until 12/20, at 0200 hours0.00231 days <br />0.0556 hours <br />3.306878e-4 weeks <br />7.61e-5 months <br />, when a Main Feedwater Pump Vent valve bonnet blew off re- -

sulting in an unisolatable steam leak. The unit load was reduced to 40% power to remove the pump from service for repairs. At 1045, af ter the unit was stabilized at 37% reactor power, a main turbine governor valve LVDT failed causing a loss o/ valve position control signal.

The resulting incorrect signal caused the turbine electro-hydraulic control system to move the associated governor valve 100% open and re-duced steam line pressure sufficiently to trip the Steam Line Break Instrumentation and Control System (SLBIC), which tripped the turbine .

and the. reactor. The. unit was placed back on line 12.9 hours1.041667e-4 days <br />0.0025 hours <br />1.488095e-5 weeks <br />3.4245e-6 months <br /> later.

The Unit operated at approximately 90% reactor power until 12/31, when at 850 the main turbine developed a high vibration, The uni t was man-ually tripped. Initial investigation revealed damage to the L-2 row of blading. Unit shutdown continued throughout the remainder of the re-port period.

".