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{{#Wiki_filter:TENNESSEE VALLEY AUTHORITY DIVISION OF POWER PRODUCTION BROWNS FERRY NUCLEAR PLANT MONTHLY OPERATING REPORT May 1, 1980-May 31, 1980 DOCKET NRSERS 50-259, 50-260, AND 50-296 LICENSE~iERS J PR-33, DPR-52, AND DPR-68 Submitted By: Plant Superintendent 8 0061 V 0503 TABLE OF CONTENTS Operations Summary~~~1 Refueling Information
{{#Wiki_filter:TENNESSEE VALLEY AUTHORITY DIVISION OF POWER PRODUCTION BROWNS FERRY NUCLEAR PLANT MONTHLY OPERATING REPORT May 1, 1980 May 31, 1980 DOCKET NRSERS   50-259, 50-260, AND 50-296 LICENSE ~iERS J   PR-33, DPR-52, AND DPR-68 Submitted By:
~~~4 Significant Operational Events Average Daily Unit Power Level.Operating Data Reports Unit Shutdowns and Power Reductions.
Plant Superintendent 8 0061 V 0503
~~~6~~~13~~~~~~~~16~~e 19 Plant Maintenance
~~~22 Outage Summary 28


0 erations Summar May 1980 The following summary describes the significant operational activities during the reporting period.In support of this summary, a chronological log of significant events is included in this report.There were fourteen reportable occurrences (plus two supplemental re-ports)reported to the NRC during the month of May.Unit i There were three scrams on the unit during the month.On May 6, the reactor scrammed due to turbine control valve fast closure from EHC pressure fluctuations.
TABLE OF CONTENTS Operations Summary                                    ~ ~ ~  1 Refueling Information                                  ~ ~ ~  4 Significant Operational Events                        ~ ~ ~  6 Average Daily Unit Power Level  .                     ~ ~ ~ 13 Operating Data Reports                      ~ ~ ~ ~ ~ ~ ~ ~ 16 Unit Shutdowns  and Power Reductions.                 ~ ~ e 19 Plant Maintenance                                      ~ ~ ~ 22 Outage Summary                                              28
The reactor scrammed on May 7, after the main and RFP turbines tripped from a false high water level signal caused by a blown fuse in the"A" feedwater inverter.On May 27, the reactor scrammed after a generator load rejection caused by the operation of the main transformer differential relay due to personnel error.Unit 2 There were three scrams on the unit during the month.On May 2, the reactor was manually scrammed to repair a leak on the main steam"B" control valve, second steam leak-off piping flange.The"reactor was manually scrammed on May 3, to repair the EHC servo-valve to the"A" turbine control valve be-cause the servo-valve had been installed incorrectly.
 
On May 16, the reactor was manually scrammed to repair an EHC oil leak in the"C" control valve servo-motor.
0  erations  Summar May 1980 The  following  summary  describes the significant operational        activities during the reporting period.        In support of this    summary,  a chronological log of significant events is included in this report.
0 erations Summar (Continued)
There were fourteen reportable occurrences        (plus two supplemental re-ports) reported to the     NRC during the month of May.
May 1980 Unit 3 There were two scrams on the unit during the month.On May 15, the reactor scrammed due to a generator load rejection when a gr'ound occurred on the gen-erator field ground detector (possible personnel error).The reactor scrammed on May 21, due to high flux on APRM"D" and MSIV"B" and"C" not fully open.Investigation revealed that the AC pilot valve on the"C" outboard MSIV did not re-energize (defective relay)during tests on the MSL high flow switches.
Unit i There were three scrams on the       unit during the   month. On May   6, the reactor   scrammed due   to turbine control valve fast closure from         EHC pressure fluctuations. The reactor scrammed   on May 7, after the main and   RFP turbines tripped from   a false high water level signal caused       by a blown fuse     in the "A" feedwater inverter.     On May   27, the reactor scrammed   after a generator load rejection caused by the operation of the main transformer           differential relay   due to personnel error.
0 erations Summary (Continued)
Unit 2 There were three scrams on the     unit during the   month. On May   2, the reactor   was manually scrammed to repair a leak on the main steam "B" control valve, second steam leak-off piping flange.         The"reactor was manually scrammed on May 3,   to repair the EHC servo-valve to the "A" turbine control valve be-cause the servo-valve had been       installed incorrectly. On May   16, the reactor was manually scrammed to repair an     EHC oil leak in the "C" control valve servo-motor.
Hay 1980 Fati ue Usa e Evaluation The cumulative usage factors for the reactor vessel are as follows: Location Usa e Factor Shell at water line Feedwater nozzle Closure studs Unit 1 Unit 2 0.00464 0.21997 0.00343 0.14835 0.19099 0.12106 Unit 3 0.00295 0.10950 0.08794 Note: This accumulated monthly information satisfies technical specification section 6.6.A.17.b(3) reporting requirements.
 
Common S stems Approximately 9.99E+04 gallons of waste liquid were discharged containing approximately 1.67E-Ol curies of activity.
0 erations Summar   (Continued)
Refuelin Information May 1980.Unit 1 Unit 1 is scheduled for its fourth refueling beginning on or about April 15, 1981, with a scheduled restart date of July 25, 1981.This re-fueling will involve loading additional 8 x 8 R (retrofit) fuel assemblies into the core, the final fix on the sparger modification, power supply on LPCI modification, and torus modifications if all approvals are received.There are 764 fuel assemblies in the reactor vessel.The spent fuel storage pool presently contains 550 spent 7 x 7 fuel assemblies, five 8 x 8 fuel assemblies, one 8 x 8 R fuel assemblies, and 20 new P 8 x 8 R assemblies.
May 1980 Unit 3 There were two scrams on the   unit during the month. On May 15, the reactor scrammed due to a generator load rejection when a gr'ound occurred on the gen-erator field ground detector (possible personnel error).       The reactor scrammed on May 21, due   to high flux on APRM "D" and MSIV "B" and "C" not   fully open.
Because of modification work to increase spent fuel pool capacity to 3471 assemblies, present capacity is limited to 1152 assemblies.
Investigation revealed that the   AC pilot valve   on the "C" outboard MSIV   did not re-energize   (defective relay) during tests   on the MSL high flow switches.
Unit 2 Unit 2 is scheduled for its third refueling beginning on or about September 1, 1980, with a scheduled restart date of October 11, 1980.Resumption of operation on that date will require a change in technical specifications pertaining to the core thermal limits.Li'censing information in support of these changes will be submitted to the NRC before the outage.This refueling involves replacing some more 7 x 7 fuel assemblies with 8 x 8 R (retrofit) assemblies, and power supply on LPCI modification.
 
There are 764 fuel assemblies in the reactor vessel.At the end of the month, there were 132 discharged cycle 1 fuel assemblies and 268 discharged cycle 2 fuel assemblies in the spent fuel storage pool.The present storage capacity of the spent fuel pool is 1080 assemblies.
0 erations Summary (Continued)
With present capacity, Refuelin Information (Continued)
Hay 1980 Fati ue Usa e Evaluation The cumulative usage factors for the reactor vessel are as follows:
May 1980 Unit 2 (Continued) the 1979 refueling would be the last refueling that could be discharged to the spent fuel pool without exceeding that capacity and maintaining full core discharge capability in the pool.Unit 3 Unit 3 is scheduled for its third refueling beginning on or about October 17, 1980, with a scheduled restart date of November 25, 1980.This EOC-3 refueling, involves loading additional 8 x 8 R (retrofit) assemblies into the core, and power supply on LPCX modification.
Location                                       Usa e Factor Unit  1          Unit  2      Unit  3 Shell at water line                 0.00464         0.00343      0.00295 Feedwater nozzle                    0.21997          0.14835      0.10950 Closure studs                        0. 19099        0.12106      0.08794 Note:     This accumulated monthly information   satisfies technical specification section 6.6.A.17.b(3) reporting requirements.
There are 764 fuel assemblies presently in the reactor vessel.There are 144 discharged cycle 2 fuel assemblies and 208 discharged cycle 1 fuel assemblies in the spent fuel storage pool.The present storage capacity of the spent fuel pool is 1528 assemblies.
Common S stems Approximately 9.99E+04 gallons of waste   liquid were discharged containing approximately 1.67E-Ol curies of   activity.
With present capacity, the 1980 refueling would be the last refueling that could be discharged to the spent fuel pool without exceeding that capacity and maintaining full core discharge capability in the pool.
 
Si nificant 0 erational Events Unit 1 Date Time Event 5/01/80 0001 Reactor thermal power at 99%, maximum flow (rod limited)sequence"A" 5/02/80 2045 2359 Reduced thermal power from 99%to 95%due to EHC high vibration Reduced thermal power from 95%to 80%for turbine C.V.test and SI's 5/03/80 0119 0230 Turbine C.V.tests and SI's completed, commenced power ascension Reactor thermal power at 95%, holding due to EHC high vibration 5/05/80 1016 1402 5/06/80 0520 Commenced power ascension from 95%thermal power Reactor thermal power at 99%, maximum flow (rod limited)Reactor scram No.124'rom 99%thermal power on (2).generator load rejection, No.6 intermediate valve closed while testing No.5 intermediate valve 5/07/80 0009 0345 0522 0546 1239 1535 1725 2002 2018 Commenced rod withdrawal Reactor critical No.144 sequence"A" Rolled T/G Synchronized generato~commenced power ascension Reactor scram No.125 from 41%thermal power, turbine trip when fuse blew in"A" feedwater in-verter and"B" feedwater high level tripped turbine and the reactor scrammed Commenced rod withdrawal Reactor critical No.145 sequence"A" Rolled T/G Synchronized generator, commenced power ascension 5/08/80 0300 0530 Commenced PCIOHR from 55%thermal power Reactor thermal power at 72%, holding remote"B" reactor feed pump for maintenance to flow indicator 5/09/80 0450 2300"B" reactor feed pump maintenance completed and pump placed in service, commenced power ascension Reactor thermal power at 77%, holding for maintenance to"C" condensate booster pump 5/11/80 0133 0215"C" condensate booster pump maintenance completed commenced power ascension Commenced PCIORM from 90%thermal power Si nificant 0 erational Events Unit 1 Date Time Event 5/11/80 2300 5/13/80 1648 1930 Reactor thermal power at 98%flow limited Commenced reducing thermal power from 98%due to high EHC vibration Reactor thermal power at 90%, holding for high EHC vibration 5/15/80 0640 0700 1315 Commenced power ascension Commenced PCIOMR from 95%thermal power Reduced thermal power from 98%to 95%due to high EHC vibration 5/16/80 1445 1500 Commenced power ascension Reactor thermal power at 99%, holding due to high EHC vibration 5/17/80 0339 0415 1500 Reduced thermal power from 99%to 80%for turbine C.V.tests and SI's Turbine C.V.tests and SI's completed, commenced power ascension Reactor thermal power at 99%, holding due to high EHC vibration 5/19/80 1426 Reduced thermal power from 99%to 95%due to high ECH vibration 5/21/80 0730 0950 Commenced power ascension from 95%thermal power Reactor thermal power at 99%, holding due to high EHC vibration 5/22/80 1500 Reactor thermal power at 99%, holding due to high EHC vibration 5/23/80 2107 2152 2209 2319 2323 Reduced thermal power from 99%to 45%for control rod sequence exchange Removed"A" recirculation pump M.G.set from service for brush replacement Reactor thermal power at 45%, commenced control rod se-quence exchange from"A" to"B""A" recirculation pump M.G.set brush replacement com-pleted and pump placed in service"B" recirculation pump M.G..set removed from service.for brush replacement 5/24/80 0130 0330 Control rod sequence exchange completed holding for brush replacement on"B" recirculation pump M.G.set"B" recirculation pump M.G.set brush replacement com-pleted and pump placed in service, commenced power as-cension Si nificant 0 erational Events Unit 1 Date Time Event 5/25/80 1405 5/27/80 0845 2001 Commenced PCIOMR from 70%thermal power Reactor thermal power at 98%, holding due to EHC high vibration (1)Reactor scram No.126 from 98%thermal power on gen-erator load reject while replacing a PR block in main transformer circuitry creating a differential and load rej ection 5/28/80 0109 0445 0625 0642 1900 Commenced rod withdrawal Reactor critical No.146 sequence Rolled T/G Synchronized generator, commenced Commenced PCIOMR from 71%thermal f lilt power ascension power 5/30/80 0030 5/31/80 2400 Reactor thermal power at 97%, EHC vibration limited Reactor thermal power at 97%, EHC vibration limited Date Time Si nificant 0 erational Events Unit 2 Event 5/01/80 0001 2206 Reactor thermal power at 98%, CPR limited sequence"A" Commenced reducing thermal power for shutdown due to steam leak in moisture separator room 5/02/80 0050 0605 1315 2036 2102 Reactor scram No.98 (manual), from 35%thermal power to accommodate repairs to steam leak Steam leak fixed, commenced rod withdrawal Reactor critical No.109 sequence"B" Rolled T/G Synchronized generator, commenced power ascension 5/03/80 0700 1830 1910 Reactor thermal power at 65%holding-No.1 control valve not open Commenced reducing thermal power for shutdown to correct No.1 control valve problems Reactor scram No.99 (manual)from 35%thermal power to accommodate control valve repairs 5/04/80 0455 0624 0938 0957 1900 No.1 control valve fixed, commenced rod withdrawal Reactor critical No.110 sequence"A" Rolled T/G Synchronized generator, commenced power ascension"Commenced PCIOMR from 70%thermal power 5/05/80 2330 5/09/80 2225 Reactor thermal power at 97%, maximum flow Reduced thermal power from 97%to 60%for control rod pattern adjustment 5/10/80 0330 Control rod pattern adjustment completed commenced PCIOMR from 60%thermal power 5/12/80 0320 5/16/80 1805 1840 2135 2330 Reactor thermal power at 98%, maximum flow Commenced decreasing thermal power for shutdown due to EHC leak (No.3 servo valve)Reactor scram No.100 (manual), from 35%thermal power to accommodate EHC maintenance EHC maintenance completed, commenced rod withdrawal Reactor critical No.111 sequence"A" 5/17/80 0301 0327 5/18/80 1440 5/19/80 0700 1840 Rolled T/G Synchronized generator, commenced power ascension Commenced PCIOMR from 92%thermal power Reactor thermal power at 99%, maximum flow Reduced thermal power from 99%to 90%for removal of"C" string high pressure heaters from service, due to FCV 6-84 flange leak 10 Date Time Si nificant 0 erational Events Unit 2 Event 5/20/80 0450 0530 2055"C" string high pressure heaters (leak)maintenance completed, commenced power ascension Commenced PCIOMR from 95%thermal power Reactor thermal power at 99%, maximum flow 5/24/80 0015 0220 1245 1500 Reduced thermal power from 99%to 80%for turbine C.V.tests and SI's Turbine C.V.tests and SI's completed Commenced PCIOMR from 95%thermal power Reactor thermal power at 99%, maximum flow 5/27/80 0736 1443 1525 1630 1930 Reduced thermal power from 99%to 90%for removal of"C" string high pressure heaters from service for maintenance (leaks)Maintenance to"C" string high pressures completed and heaters placed in service Commenced power ascension from 90%thermal power Commenced PCIOMR from 95%thermal power Reactor thermal power at 99%, maximum flow 5/31/80 2400 Reactor thermal power at 99%, maximum flow Date Time Si nificant 0 erational Events Unit 3 Event 5/01/80 0001 Reactor thermal power at 99%, maximum flow (rod limited)Sequence"A" 5/02/80 0700 5/03/80 0725 1440 1600 Reactor thermal power at 99%, maximum flow (rod limited)Reduced thermal power from 98%to 50%, tachometer main-tenance on"B" recirculation pump"B" recirculation pump tachometer maintenance completed and pump placed in service, commenced power ascension Commenced PCIOMR from 62%thermal power 5/06/80 0030 5/09/80 2330 Reactor thermal power at 99%, maximum flow (rod limited)Reduced thermal power from 99%to 85%for turbine C.V.tests and SI's 5/1O/SO 0200 0700 Turbine C.V.tests and SI's completed, commenced PCI(MR from 85%thermal power Reactor thermal power at 99%, maximum flow 5/15/so o7oo 0815 1800 2027 2229 2245 Reduced thermal power from 99%to 70%to perform SI 4.2.A-3 (reactor low y~ter level)Reactor scram No.82 , load reject due to generator field ground Commenced rod withdrawal Reactor critical No.92 sequence"A" Rolled T/G Synchronized generator, commenced power ascension 5/16/80 0930 5/18/80 1500 2150 Commenced PCIOMR from 65%thermal power Reactor thermal power at 98%, (rod limited)Reduced thermal power from 98%to 55%for control rod pattern adjustment 5/19/80 0005 1800 Control rod pattern adjustment completed, commenced power ascension Commenced PCIOMR from 85%thermal power 5/20/80 2300 5/21/80 1348 1944 2205 Reactor thermal power at 99%, (rod limited)Reactor scram No.83 from 99%thermal power while (2)testing of main steam line high flow switches per instruction 4.2.A.7 Commenced rod withdrawal Reactor critical No.93 sequence"A" 5/22/80 0031 0051 1630 Rolled T/G Synchronized generator, commenced power ascension Commenced PCIOMR from 75%thermal power Si nificant 0 erational Events Unit 3 Date Time Event 5/23/80 2300 5/24/80 2125 2235 2335 Reactor thermal power at 99%, (rod limited)Commenced reducing thermal power for control rod pattern adjustment Reactor thermal power at 55%, holding for control rod pattern adjustment Removed"A" recirculation pump M.G.set from service for brush replacement 5/25/80 0245 0252 0310 0415 0430 1315-1830"A" recirculation pump M.G.set brush replacement com-.pleted and pump placed in service Removed"B" recirculation pump M.G.set from service for brush replacement Control rod pattern adjustment completed holding for brush replacement on"B" recirculation pump M.G.set"B" recirculation pump M.G.set brush replacement and pump placed in service, commenced power ascension Reactor thermal power at 68%, holding due to"C" main steam line isolation Commenced power ascension Commenced PCIOMR from 70%thermal power 5/27/80 0030 5/30/80 2200 Reactor thermal power at 99%, (rod limited)Reduced thermal power from 99%to 50%for control rod sequence exchange from"A" to"B"~5/31/80 0815 2400 Control rod'equence exchange completed, commenced power ascension Reactor thermal power at 84%, power ascension in progress (1)(2)Personnel Error Equipment malfunction 13 AVERAGE DAILY UNIT POWER LEVEL DOCKET NO.UNIT DATE 5-1-80 COMPLETED BY TELEPHONE 205-729-6846 MONTH DAY AVERAGE DAILY POWER LEVEL (il(We-Net)
Refuelin   Information May 1980.
I 1064 DAY AVERAGE DAILY POWER LEVEL (MWe iVet)24 17 4 10 13 14 IS 16 1063 750 835 1014 1071 1076 1078 1077 1070 1071 1083 1072 1072 358 703 18 19 20 21 22 23 24 25 26 27 28 29 30 31 999 832 1033 607 666 974 1023 685 957 1071 1064 1082 1027 780 INSTRUCTIONS Qn this format, list the average daily unit power level in ilDVe.i/et for each day in the reporting month.Compute to the nearest whole megawatt.(')(77) 14 AVERAGE DAlLY UNIT POWER LEVEL'I DOCKET NO.DATE COilIPLETED BY Browns Ferry-1 5-1-80 Don Green TELEPHONE 205-729-6846 DAY AVERAGE DAlLY POWER LEVEL (i%I We-Net)DAY AVERAGE DAlLY POWER LEVEL (iHWe-Net) 17 1060 4 10 12 13 15 16 1054 1014 1026 1037 228 189 713 799 790 1008 1042 1012 968 1005 1047 18 19 20 21 22 23 25 26 27 28 29 30 31 1026 1042 1023 1040 1067 988 558 679 879 859 908 1052 1031 INSTRUCTIONS On this format, list the average daily unit power level in illWe-Net for each day in the reporting month.Compute to the nearest whole megawatt.(9 j77) 15 AVERAGE DAILY UNIT POWER LEVEL DOCKET NO.DATE Browns Ferry-2 COMPLETED BY Don Green TELEPHOiNE MONTH DAY AVERAGE DAILY POWER LEVEL (M We-Net)1 0 DAY AVERAGE DAILY POWER LEVEL (MWe-Net)560'7 4 10 12 13 15-16 38 503 384 954 1043 1047 1043 1027 732'23 1064 1066 1061 1068 828 18 19 20 21 22 23 24 25 26 27 28 29 30 31 913 1043 1038 1060 1086 1059 1027 1070 1058 ,1023 1055 1044 1039 1034 INSTRUCTIONS On this format, list the average daily unit power level in MIVe.Net for each day in the reporting n\onth.Compute to the nearest whole megawatt.(')(77)~,~
Unit 1 Unit 1 is scheduled   for its fourth refueling beginning         on or about April 15,   1981, with a scheduled   restart date of July     25, 1981. This re-fueling   will involve   loading additional     8 x 8 R (retrofit) fuel   assemblies into the core, the final     fix on the sparger modification, power supply on LPCI modification,   and   torus modifications     if all approvals   are received.
16 OPERATING STATUS OPERATING DATA REPORT DOCKET NO~0-2 DATE 6-1-80 CO41IPLETED BY Green TELEPHONE-846 Notes Browns Ferrv-Unit 1 2.Reporting Period: 3.Licensed Thermal Power (41IWt): 4.Nameplate Rating (Gross 49IWe): 5.Design Electrical Rating (Net 4%We): 6.Maximum Dependable Capacity (Gross 41OVe): 7.Ifavimum De endableCa acit Net MWe: p p y()8.If Changes Occur in Capacity Ratings (Items Number 3 Through 7)Since Last Report, Give Reasons: N A 9.Power Level To Which Restricted, If Any (Net iWIWe): IO.Reasons For Restrictions.
There are 764   fuel assemblies in the reactor vessel.           The spent   fuel storage pool presently contains 550 spent         7 x 7 fuel assemblies, five     8 x 8 fuel assemblies,   one 8 x 8 R fuel assemblies,     and 20 new   P 8 x 8 R assemblies.
If Any: This Month Yr:to-Date Cumuhtive 11.Hours In Reporting Period 12.Number Of Hours Reactor Was Critical 13.Reactor Reserve Shutdown Hours 14.Hours Generator On-Line~15.Unit Reserve Shutdown Hours 16.Gross Thermal Energy Generated (MWH)17.Gross Electrical Energy Generated (MWH)18.Net Electrical Energy Generated (MWH)19.Unit Service Factor 20.Unit Avaihbility Factor 21.Unit Capacity Factor (Using 44IDC Net)22.Unit Capacity Factor (Using DER Net)23.Unit Forced Outage Rate 24.Shutdowns Scheduled Over Next 6 41fonths 744'647 51 145 708.08 35.92 701.23 0 1531.68 283.85 1428.60 0 29808.96 4973.29,041.33 0 2,075,263 3,816,795 77,953,288 25 771 850 663,602 94.3.94.3 83.8 83.8 5.7 1,213,207 39.2 39.2 31.2 31.2 18.8 25,015,175 56.8 56.8.45.9 45.9 32.4 (Type, Date, and Duration of Each): 680 430 2 253 390 25.If Shut Down At End Of Report Period, Estimated Date of Startup: 26.Units In Test Status (Prior to Commercial Operation):
Because   of modification work to increase spent fuel pool capacity to             3471 assemblies,   present capacity is limited to 1152 assemblies.
Forecast Achieved INITIAL CRITICALITY INITIA L ELECTRICITY COMMERCIAL OPERATION~I~3 j~~,q~,>~M'a i'i." (9/77) 17 OPERATING DATA REPORT DOCKET NO.50-260 DATE~E}COtlfPLETED BY 2'~~TELEPHONE~~8-6846 OPERATING STATUS Notes Browns Ferr-finest 2 2.Reporting Period: 3.Licensed Thermal Power (MWt): 4.Nameplate Rating (Gross tlf We): 1152 5.Design Electrical Rating (Net MWe): 6.tlfaximum Dependable Capacity (Gross tbfWe): 'um De e dable Ca acit Net idWe: 1098.4 1065 7..faxm p n p y()8.If Changes Occur in Capacity Ratings (Items Number 3 Through 7)Since Last Report, Give Reasons: 9.Power Level To Which Restricted, If Any (Net tlfWe): ,"10.Reasons For Restrictions.
Unit 2 Unit 2 is scheduled   for its third refueling beginning       on or about September   1, 1980, with a scheduled     restart date of October       11, 1980.
If Any r This Month Yr.-to-Date Cumulative 744 3 647-715.52 28.48-.11.Hours In Reporting Period 12.Number Of Hours Reactor Was Critical 3 146.60 13.Reactor Reserve Shutdown Hours 14.Hours Geherator On.Line 15.Unit Re~rve Shutdown flours 0 0 16.Gross Thermal Energy Generated (MWH)2 120 551 8 781g400 ty.Gross Eteetrieal Energy Generated (ittyH)~y>>g>O 2 936 690 18.Net Electrical Energy Genersated (MWH)19.Unit Service Factor 94.1 84.1 20.Unit'vailability Factor 94.1 84.1 21.Unit Capacity Factor (Using tlfDC Net)87.6 73.6 22.Unit Capacity Factor (Using DER Net)87.6 73.6 23.Unit Forced Outage Rate 59'59 24.Shutdowns Scheduled Over Next 6 Months (Type, Date.and Duration of Each): 46'0 6 27 631.08~12,275.34 0 74 936 400 24 886 758 24 189 526 8.0 58.0.49.3 49.3 35.0 25.If Shut Down At End Of Report Period, Estimated Date of Startup: 26.Units In Test Status (Prior to Commercial Operation):
Resumption of operation on       that date will require     a change in technical specifications pertaining to the core thermal limits. Li'censing information in support of these     changes   will be submitted to the     NRC before the outage.
Forecast Achieved INITIAL CRITICALITY INITIAL ELECTRICITY COtlf M ERCIA L OPER ATION 18 OPERATING DATA REPORT OPERATliVG STATUS DOCKET NO.50-296 DATE 6-1-80 COi'IPLETED BY~~~e TELEPHONE~~2-846 Notes l.Unit Name: Browns Ferr-Unit 3 2.Reporting Period:~3.Licensed Thermal Power (ilOVt): 4.Nameplate Rating (Gross iaaf tVe);1152 5.Design Electrical Rating (Net MWe): 6.hfaximum Dependable Capacity (Gross AIWe): 1098-4 um De endableCa acit Net iiOVe: 7.,faxmi p p y ()8.If Changes Occur in Capacity Ratings (Items Number 3 Through 7)Since Last Report.Give Reasons: N/A 9.Power Level To Which Restricted, If Any (Net ilfWe): 10.Reasons For Restrictions, If Any: This Month Yr.-to Date 3 647 744 11.Hours In Reporting Period 12.Number Of Hours Reactor Was Critical 13.Reactor Reserve Shutdown Hours 14.Hours Generator On-Line 15.Unit Reserve Shutdown IIours 16.Gross Thermal Energy Generated (MWH)17.Gross Electrical Energy Generated (MWH)18.Net Electrical Energy Generated (MPH)19.Unit Service Factor 20.Unit Availability Factor 21.Unit Capacity Factor (Using i9ifDC Net)2"".Unit Capacity Factor (Using DER Net)23.Unit Forced Outage Rate 24.Shutdowns Scheduled Over iVext 6 Months (Refuel Outa e October 1980 3214.95 20.48 3186.38 723.52 20.48 718.45 0 0 2 139 84 9 947 427 3 356 390 718 180 700 399.3,272,840 87.4 6.6 84.3 88.4 84.3 12.6 3.4 Type, Date,and Duration of Each): Cumulative 28 511 22122.50 1678.79 21624.'19 0'3 055 293 20 758 970 20,160,613 75.8'6.4 66.4 9.6 25.If Shut Down At End Of Report Period.Estimated Date of Startup: 26.Units ln Test Status (Prior,to Commercial Operation):
This refueling involves replacing       some more 7     x 7 fuel assemblies with 8 x 8 R (retrofit) assemblies,   and power supply on LPCI       modification.
Forecast Achieved IN IT I A L CRITICA LIT Y INITIAL ELECTRICITY COMM ERCIA L OPER ATIOi I (9/77)
There are 764   fuel assemblies in the reactor vessel.         At the end of the month, there were 132 discharged       cycle 1   fuel assemblies   and 268 discharged cycle   2 fuel assemblies in the spent fuel storage pool.           The present storage capacity of the spent fuel pool is 1080 assemblies.             With present capacity,
UNIT SIIUTDOWNS AND POWER REDUCTIONS DOCKET NO.UNIl NAhIE DATE COhIPLETED BY TELEPI lONE 50-259 Browns Ferr-1 5-1-80 205-729-6846 No.Date m~lY Licenscc Eve>>l Report 4 4J 0 D Q Cause k.Corrective Actlotl to Prevent Rccurrcnce 122 800506 24.44 B Generator load rejection (No.6 intermediate valve closed while testin No.5 intermediate valve.123 800507 7.65 A Turbine trip due to a blown fuse in"A" feedwater inverter and"B" feedwater hi h level si nal.124 800523 Derated for control rod sequence exchan e.125 800527 10.68 Generator load rejection while re-placing a PK block in ma$n trans-former creating a differhntial and load re ection (ersonnel error I F: Forced': Scheduled"~'-(9/77)~t Reason: A-Equipment Failure (Explain)B.hlaintenance or Test C-Refueling D.Regulatory Restriction E.Operator Training 8;Liccnsc Exa>>tination F-Administrative G-Operational Error (Explain)'I Other (Explain)hIethod: I-hlanual 2-h(anual Scram.3-Aulotnatic Scram.4.Other (Explain)4 Exhibit G-Instructions for Preparation of Data Entry Sheets I'or l.iccnsec Evc>>t Rcport (I.ER)File (NURFG-OI 6I)5 Exl)ibit I-Sr>>>>c Source UNIT SIIUTDOWNS AND POWER REDUCTIONS REPORT hiON Ill~Ha DOCKET NO.UNIT NAhl E DATE COhIPLETED BY TELEPI!ONE 50-260 Browns Ferr-2 o Cree 205-729-6846 Date I IA r$CP Liccnscc Event Rcport¹CO CP 41 v)G 4J~O C Q i u 0 Cause&Corrective Aclion to Prevent Rccurrcnce 136 800502 F 20.21 A To accommodate repairs to steam leak in steam tunnel.137 800503 F 14.78 A To accommodate repairs to No.1 control valve.138 800509 Derated for control rod pattern ad ustment.139 800516 8.78 A To accommodate repairs to EHC leak No.3 servo valve.I F: Forced S: Scheduled (9/77)-i'i~Reason: A.Equipment Failure (Explain)B-hlaintenance or Test C-Refueling D.Regulatory Restriction E.Operator Training&Liccnsc Exanlination
 
, F-Administrative
Refuelin   Information (Continued)
~G-Opcfattunal Error (Explain)~I I-Other (Explain)Method: I-hlanual 2.hlanual Scram.3-Automatic Scram.4.0llter (Explain)Exhibit G-Instructions for Preparation of Data Entry Sheets fur l.iccnsee Event Report (I.L'R)File (NUREG-OI6I)Exhibit I-Sante Source UNIT SIIUTDOWNS AND POWER REDUCTIONS DOCKET NO.UNIT NAhlE DATE COhlPLETED IIY TELEPIIONE 50-296 Browns Ferr-3 5-1-80 205-729-6846 N((.Date r(IX (J (P A J~(/I Lice nscc Event Report~((('n IA cn'Cr Cl O Q Q O Cause&.Corrective A>>lion to Prevent Rccurrcnce 123 800503 Derated for maintenance on"B" recirculation pump.124 800515 14.50 G Apparent generator field ground-(personnel error).125 800518 H Derated for control rod pattern adjustment.
May 1980 Unit 2 (Continued) the 1979 refueling would be the     last refueling that could     be discharged   to the spent fuel pool without exceeding that capacity and maintaining           full core discharge capability     in the pool.
126 , 800521 11.05 B Reactor scrammed while performing reactor low water level SI.127 800524 Derated for control rod pattern adjustment.
Unit 3 Unit 3 is scheduled for its third refueling beginning       on or about October 17, 1980, with a scheduled       restart date of   November 25, 1980. This EOC-3   refueling, involves loading additional       8 x 8 R (retrofit) assemblies into the core,   and power supply on LPCX   modification.
128 800530 S Derated for control rod sequence exchange., F: Forced': Scheduled (()/77).Reason: A-Equipment Failure (Explain)B-hlaintenance or Test C-Refueling D Regulatory Restriction E.Operator Training&.Ucensc Examination F.Adnlinist ra tive G-Operational Error (Explain)'
There are 764   fuel assemblies presently in the reactor vessel.           There are 144 discharged cycle     2 fuel assemblies   and 208 discharged   cycle 1 fuel assemblies   in the spent fuel storage pool. The present storage capacity of the spent fuel pool is 1528 assemblies.         With present capacity, the 1980 refueling would   be the last refueling that could     be discharged   to the spent fuel pool without exceeding that capacity       and   maintaining full core discharge capability in the pool.
I I Other (Explain)hlethod: I-hlanual 2-hlanual Scram.3-Autonlatic Scraln.4.Other (Explain)Exhibit G-Instructions for Preparation of Data Entry Shc>>ts for l.icensee Event Report (I.l(R)Fil>>(NUREG-OI 6 I)Exhibit I-Sa(n>>Source CSSC 1:.UIPMFNT BR011NS,FERRY NUCLEAR PIANT UNIT 2 11ECHANICAL MAINTENANCE SUM 1ARY For the Month of May]9 80 DATE SYSl~rii COMPONENT EFFECT ON SAFE NATURE OF OPERATION OF MAINTENANCE THE REACTOR CAUSE OF MALFUNCTION RESULTS OF MALFUNCTION ACTION TAKEN TO PRECLUDE RECURRENCE 5/15/8 HPCI Instrument line FE 73-33 Instrument lin sags and clamp missing None Clamps missing Inoperable instrument line Replaced and tightened clamps TR 103607 CSSC E UIPHENT WINS FERRY NUCLEAR PLANT UNIT f fECflANICAL MAINTENANCE SUMfARY For the Month of.Ma/19 80 DATE SYS'1i;if.
 
COMPONENT EFFECT ON SAFE NATURE OF OPERATION OF ffAINTENANCE THE REACTOR CAUSE OF MALFUNCTION RESULTS OF MALFUNCTION ACTION TAKEN TO PRECLUDE RECURRENCE 5/15/8 FPC 3A pump Packing leak None Packing leak Packing leak Tightened packing TR 182948 CSSC E UIPMENT BROWNS FERRY NUCLEAR PLANT UNIT'5KQIANICAL MAINTENANCE
Si nificant 0   erational Events Unit   1 Date     Time                               Event 5/01/80 0001     Reactor thermal power at 99%, maximum flow (rod limited) sequence "A" 5/02/80   2045     Reduced   thermal power from     99% to 95% due to EHC high vibration 2359      Reduced thermal power from 95%       to 80% for turbine   C.V.
test and SI's 5/03/80   0119     Turbine C.V. tests and SI's completed, commenced power ascension 0230      Reactor thermal power at 95%, holding due to EHC high vibration 5/05/80   1016     Commenced   power ascension from 95% thermal power 1402      Reactor thermal power at 99%, maximum flow (rod limited) 5/06/80  0520      Reactor scram No. 124 (2).'rom 99% thermal power on generator load rejection, No. 6 intermediate valve closed while testing No. 5 intermediate valve 5/07/80   0009     Commenced rod withdrawal 0345      Reactor critical No. 144 sequence "A" 0522      Rolled T/G 0546      Synchronized generato~ commenced power ascension 1239      Reactor scram No. 125         from 41% thermal power, turbine trip when fuse blew in "A" feedwater in-verter and "B" feedwater high level tripped turbine and the reactor scrammed 1535      Commenced rod withdrawal 1725      Reactor critical No. 145 sequence "A" 2002      Rolled T/G 2018      Synchronized generator, commenced power ascension 5/08/80 0300     Commenced   PCIOHR from 55% thermal power 0530      Reactor thermal power at 72%, holding remote "B" reactor feed pump for maintenance to flow indicator 5/09/80 0450     "B" reactor feed pump maintenance completed and pump placed in service, commenced power ascension 2300      Reactor thermal power at 77%, holding for maintenance to "C" condensate booster pump 5/11/80 0133     "C" condensate     booster pump   maintenance   completed commenced   power ascension 0215      Commenced   PCIORM from 90%   thermal power
 
Si nificant 0 erational Events Unit   1 Date   Time                               Event 5/11/80 2300 Reactor thermal power at     98%   flow limited 5/13/80 1648  Commenced   reducing thermal power from     98% due to high EHC vibration 1930  Reactor thermal power at 90%, holding       for high EHC vibration 5/15/80 0640 Commenced   power ascension 0700  Commenced   PCIOMR from 95%   thermal power 1315  Reduced thermal power from     98% to 95% due to high   EHC vibration 5/16/80 1445 Commenced   power ascension 1500  Reactor thermal power at 99%, holding due to high         EHC vibration 5/17/80 0339 Reduced thermal power from 99% to 80% for turbine C. V.
tests and SI's 0415  Turbine C. V. tests and SI's completed, commenced power ascension 1500  Reactor thermal power at 99%, holding due to high         EHC vibration 5/19/80 1426 Reduced   thermal power from   99%   to 95% due to high ECH vibration 5/21/80 0730 Commenced   power ascension from 95% thermal power 0950  Reactor thermal power at 99%, holding due to high         EHC vibration 5/22/80 1500 Reactor thermal power at 99%, holding due to high         EHC vibration 5/23/80 2107 Reduced   thermal power from     99% to 45% for control rod sequence   exchange 2152  Removed   "A" recirculation pump M. G. set from service for brush replacement 2209 Reactor thermal power at 45%, commenced control rod se-quence exchange from "A" to "B" 2319 "A" recirculation pump M. G. set brush replacement com-pleted and pump placed in service 2323 "B" recirculation pump M. G.. set removed from service.
for brush replacement 5/24/80 0130 Control rod sequence exchange completed holding for brush replacement on "B" recirculation pump M. G. set 0330 "B" recirculation pump M. G. set brush replacement com-pleted and pump placed in service, commenced power as-cension
 
Si nificant 0 erational Events Unit 1 Date   Time                             Event 5/25/80 1405 Commenced PCIOMR   from 70% thermal power 5/27/80 0845 Reactor thermal power at 98%, holding due to EHC high vibration 2001 Reactor scram No. 126 (1) from 98% thermal power on gen-erator load reject while replacing a PR block in main transformer circuitry creating a differential and load rej ection 5/28/80 0109 Commenced rod withdrawal 0445 Reactor critical No. 146 sequence f lilt 0625 Rolled T/G 0642 Synchronized generator, commenced power ascension 1900 Commenced PCIOMR from 71% thermal power 5/30/80 0030 Reactor thermal power at 97%,     EHC vibration limited 5/31/80 2400 Reactor thermal power at     97%, EHC vibration limited
 
Si nificant   0 erational Events Unit 2 Date    Time                                Event 5/01/80 0001   Reactor thermal power at 98%, CPR limited sequence "A" 2206  Commenced reducing thermal power for shutdown due to steam leak   in moisture separator     room 5/02/80 0050   Reactor scram No. 98 (manual), from         35% thermal power to accommodate repairs to steam leak 0605  Steam leak fixed, commenced rod withdrawal 1315  Reactor   critical   No. 109 sequence   "B" 2036  Rolled T/G 2102  Synchronized generator,     commenced   power ascension 5/03/80 0700   Reactor thermal power at     65%   holding   No. 1 control valve not open 1830  Commenced reducing thermal power for shutdown to correct No. 1 control valve problems 1910  Reactor scram No. 99 (manual) from 35% thermal power to accommodate control valve repairs 5/04/80 0455   No. 1 control valve fixed, commenced rod withdrawal 0624  Reactor critical No. 110 sequence "A" 0938  Rolled T/G 0957  Synchronized generator, commenced power ascension 1900  "Commenced PCIOMR from 70% thermal power 5/05/80 2330   Reactor thermal power at       97%, maximum   flow 5/09/80  2225  Reduced thermal power from 97%       to 60% for control rod pattern adjustment 5/10/80 0330   Control rod pattern adjustment completed         commenced PCIOMR   from 60% thermal power 5/12/80 0320   Reactor thermal power at 98%, maximum flow 5/16/80  1805  Commenced   decreasing thermal power for shutdown due to EHC leak (No. 3 servo valve) 1840  Reactor scram No. 100 (manual), from 35% thermal power to accommodate EHC maintenance 2135  EHC maintenance completed, commenced rod withdrawal 2330  Reactor   critical   No. 111 sequence   "A" 5/17/80   0301 Rolled T/G 0327  Synchronized generator,     commenced   power ascension 5/18/80  1440  Commenced   PCIOMR   from 92%   thermal power 5/19/80  0700  Reactor thermal power at 99%, maximum flow 1840  Reduced thermal power from 99% to 90% for removal of "C" string high pressure heaters from service, due to FCV 6-84 flange leak
 
10 Si nificant 0 erational Events Unit 2 Date    Time                            Event 5/20/80 0450 "C" string high pressure heaters (leak) maintenance completed, commenced power ascension 0530 Commenced PCIOMR from 95% thermal power 2055 Reactor thermal power at 99%, maximum flow 5/24/80 0015 Reduced thermal power from 99% to 80% for turbine C. V. tests and SI's 0220 Turbine C. V. tests and SI's completed 1245 Commenced PCIOMR from 95% thermal power 1500 Reactor thermal power at 99%, maximum flow 5/27/80 0736 Reduced thermal power from 99% to 90% for removal of "C" string high pressure heaters from service for maintenance (leaks) 1443 Maintenance to "C" string high pressures completed and heaters placed in service 1525 Commenced power ascension from 90% thermal power 1630 Commenced PCIOMR from 95% thermal power 1930 Reactor thermal power at 99%, maximum flow 5/31/80 2400 Reactor thermal power at 99%, maximum flow
 
Si nificant 0 erational Events Unit 3 Date    Time                            Event 5/01/80 0001 Reactor thermal power at 99%, maximum flow (rod limited)
Sequence "A" 5/02/80 0700 Reactor thermal power at 99%, maximum flow (rod limited) 5/03/80 0725 Reduced thermal power from 98% to 50%, tachometer main-tenance on "B" recirculation pump 1440 "B" recirculation pump tachometer maintenance completed and pump placed   in service, commenced power ascension 1600 Commenced PCIOMR from 62% thermal power 5/06/80 0030 Reactor thermal power at 99%, maximum flow (rod limited) 5/09/80 2330 Reduced thermal power from 99% to 85%     for turbine C. V.
tests and SI's 5/1O/SO 0200 Turbine C. V. tests and SI's completed, commenced PCI(MR from 85% thermal power 0700 Reactor thermal power at 99%, maximum flow 5/15/so o7oo Reduced thermal power from 99% to 70% to perform SI 4.2.A-3 (reactor low y~ter level) 0815 Reactor scram No. 82     , load reject due to generator field ground 1800 Commenced rod withdrawal 2027 Reactor critical No. 92 sequence     "A" 2229 Rolled T/G 2245 Synchronized generator,   commenced power ascension 5/16/80 0930 Commenced PCIOMR from 65%   thermal power 5/18/80 1500 Reactor thermal power at 98%, (rod limited) 2150 Reduced thermal power from 98% to 55% for control rod pattern adjustment 5/19/80 0005 Control rod pattern adjustment completed,     commenced power ascension 1800 Commenced PCIOMR from 85%   thermal power 5/20/80 2300 Reactor thermal power at 99%, (rod limited) 5/21/80 1348 Reactor scram No. 83 (2) from 99% thermal power while testing of main steam line high flow switches per instruction 4.2.A.7 1944 Commenced rod withdrawal 2205 Reactor critical No. 93 sequence   "A" 5/22/80 0031 Rolled T/G 0051 Synchronized generator, commenced power ascension 1630 Commenced PCIOMR from 75% thermal power
 
Si nificant 0 erational Events Unit 3 Date   Time                                   Event 5/23/80 2300       Reactor thermal power at     99%, (rod limited) 5/24/80 2125      Commenced reducing thermal power for control rod pattern adjustment 2235      Reactor thermal power at 55%, holding for control rod pattern adjustment 2335      Removed "A" recirculation pump M.G. set from service for brush replacement 5/25/80 0245       "A" recirculation pump M.G. set brush replacement com-
                    .pleted and pump placed in service 0252      Removed "B" recirculation pump M.G. set from service for brush replacement 0310      Control rod pattern adjustment completed holding for brush replacement on "B" recirculation pump M.G. set 0415      "B" recirculation pump M.G. set brush replacement and pump placed in service, commenced power ascension 0430      Reactor thermal power at 68%, holding due to "C" main steam line isolation 1315-      Commenced power ascension 1830      Commenced PCIOMR from 70% thermal power 5/27/80 0030       Reactor thermal power at 99%, (rod limited) 5/30/80 2200      Reduced thermal power from 99% to 50%       for control rod sequence exchange from "A"   to "B"
~ 5/31/80 0815       Control rod'equence     exchange   completed, commenced power ascension 2400      Reactor thermal power at     84%, power   ascension in progress (1)     Personnel Error (2)     Equipment malfunction
 
13 AVERAGE DAILYUNIT POWER LEVEL DOCKET NO.
UNIT DATE     5-1-80 COMPLETED BY TELEPHONE       205-729-6846 MONTH DAY       AVERAGE DAILYPOWER LEVEL                              DAY        AVERAGE DAILYPOWER LEVEL (il(We-Net)                                                     (MWe iVet)
I              1064                                            17                24 1063                                             18                999 750                                             19 832 4              835                                             20                1033 1014                                                               607 21 1071                                                               666 22 1076                                           23                974 1078                                                               1023 24 1077                                           25                685 10 1070                                                               957 26 1071                                            27                1071 1083                                                               1064 28 13 1072                                           29                1082 1072                                                               1027 14                                                              30 IS              358                                             31                 780 16              703 INSTRUCTIONS Qn this format, list the average daily unit power level in ilDVe.i/et for each day in the reporting month. Compute to the nearest whole megawatt.
(')(77)
 
14 AVERAGE DAlLYUNIT POWER LEVEL
                                                                                'I DOCKET NO.
Browns   Ferry-1 DATE      5-1-80 COilIPLETED BY        Don Green TELEPHONE         205-729-6846 DAY       AVERAGE DAlLYPOWER LEVEL                              DAY      AVERAGE DAlLYPOWER LEVEL (i%IWe-Net)                                                   (iHWe-Net) 17               1060 1054                                             18              1026 1014                                             19 1042 1026                                                               1023 4                                                              20 1037                                             21 1040 228                                                               1067 22 189                                                               988 23 713                                                               558 799                                                               679 25 10            790                                               26              879 1008                                                               859 27 12 1042                                             28 1012                                                               908 13                                                                29 968                                                               1052 30 1005                                                               1031 15                                                                31 16              1047 INSTRUCTIONS On this format, list the average daily unit power level in illWe-Net for each day in the reporting month. Compute to the nearest whole megawatt.
(9 j77)
 
15 AVERAGE DAILYUNIT POWER LEVEL DOCKET NO.
Browns   Ferry-2 DATE COMPLETED BY         Don Green TELEPHOiNE MONTH DAY       AVERAGE DAILYPOWER LEVEL                              DAY        AVERAGE DAILYPOWER LEVEL (MWe-Net)                                                   (MWe-Net) 1      0                                                              560   '7 38                                              18                    913 503                                            19 1043 4             384                                                                   1038 20 954                                             21                    1060 1043                                           22                    1086 1047                                                                 1059 23 1043 24                    1027 1027                                           25                    1070 10              732'23                                         26 1058 27                    ,1023 1064                                                                 1055 12                                                              28 1066                                                                 1044 13                                                              29 1061                                                                   1039 30 1068                                                                 1034 15                                                              31
-16              828 INSTRUCTIONS On this format, list the average daily unit power level in MIVe.Net for each day in the reporting n\onth. Compute to the nearest whole megawatt.
(')(77)
                                                                                                                          ~, ~
 
16 OPERATING DATA REPORT DOCKET NO     ~0-2 DATE     6-1-80 CO41IPLETED BY           Green 846 TELEPHONE OPERATING STATUS Browns Ferrv Unit 1                                 Notes
: 2. Reporting Period:
: 3. Licensed Thermal Power (41IWt):
: 4. Nameplate Rating (Gross 49IWe):
: 5. Design Electrical Rating (Net 4%We):
: 6. Maximum Dependable Capacity (Gross 41OVe):
: 7. Ifavimum De p endableCa p acit y(Net MWe:   )
: 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons:
N A
: 9. Power Level To Which Restricted,     If Any (Net iWIWe):
IO. Reasons For Restrictions. If Any:
This Month           Yr:to-Date         Cumuhtive
                                                                              '
: 11. Hours In Reporting Period                           744                          647          51 145
: 12. Number Of Hours Reactor Was Critical                 708.08                    1531.68          29808.96
: 13. Reactor Reserve Shutdown Hours 35.92                    283.85          4973.
: 14. Hours Generator On-Line                             701.23                    1428.60          29,041.33
~
: 15. Unit Reserve Shutdown Hours                         0                        0                0
: 16. Gross Thermal Energy Generated (MWH)                 2,075,263                3,816,795        77,953,288
: 17. Gross Electrical Energy Generated (MWH)             680 430                  2 253 390        25 771 850
: 18. Net Electrical Energy Generated (MWH)               663,602                  1,213,207        25,015,175
: 19. Unit Service Factor                                 94.3.                    39. 2            56.8
: 20. Unit Avaihbility Factor                             94.3                      39. 2            56. 8.
: 21. Unit Capacity Factor (Using 44IDC Net)               83. 8                    31. 2            45.9
: 22. Unit Capacity Factor (Using DER Net)                 83. 8                    31. 2            45.9
: 23. Unit Forced Outage Rate                             5.7                      18.8            32.4
: 24. Shutdowns Scheduled Over Next 6 41fonths (Type, Date, and Duration      of Each):
: 25. If Shut Down At End Of Report Period, Estimated Date        of Startup:
: 26. Units In Test Status (Prior to Commercial Operation):                          Forecast            Achieved INITIALCRITICALITY INITIAL ELECTRICITY
                                                                                                                          ~ I COMMERCIAL OPERATION
                                                                                                                                ~ 3 j ~                    ~ ,q ~ ,
                                          >~ M
                                                                                                          '  a i' i." (9/77)
 
17 OPERATING DATA REPORT 50-260 DOCKET NO.
DATE COtlfPLETED BY
                                                                                                              ~E}
2'~~
TELEPHONE  ~~8-6846 OPERATING STATUS Notes Browns    Ferr      finest 2
: 2. Reporting Period:
: 3. Licensed Thermal Power (MWt):
1152
: 4. Nameplate Rating (Gross tlfWe):
: 5. Design Electrical Rating (Net MWe):
: 6. tlfaximum Dependable Capacity (Gross tbfWe):        1098. 4 7..faxm'um De p e n dable Ca p acit y(Net idWe:)        1065
: 8. IfChanges Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons:
: 9. Power Level To Which Restricted,    If Any (Net tlfWe):
,"10. Reasons For Restrictions. If Any r
This Month            Yr.-to-Date         Cumulative
  -.11. Hours  In Reporting Period                              744                  3 647              46'0    6
: 12. Number Of Hours Reactor Was Critical
                                                            -  715.52                3 146.60          27  631.08 Reactor Reserve Shutdown Hours 28.48                                  ~ 12,275.34 13.
: 14. Hours Geherator On. Line
: 15. Unit Re~rve Shutdown flours                            0                    0                  0 2 120 551            8 781g400          74 936 400
: 16. Gross Thermal Energy Generated (MWH) ty. Gross Eteetrieal Energy Generated (ittyH)         ~y>>        g>O            2  936 690          24 886 758 24 189 526
: 18. Net Electrical Energy Genersated (MWH)
: 19. Unit Service Factor                                    94. 1                84. 1                8.0 Unit'vailability Factor                                94. 1                84. 1              58.0  .
                                                                          '59 20.
: 21. Unit Capacity Factor (Using tlfDC Net)                 87. 6                73.6                49.3
: 22. Unit Capacity Factor (Using DER Net)                   87.6                  73.6                49.3
: 23. Unit Forced Outage Rate                                59                                        35.0
: 24. Shutdowns  Scheduled  Over Next  6 Months  (Type,  Date. and Duration of Each):
: 25. IfShut Down At End Of Report Period, Estimated Date          of Startup:
: 26. Units In Test Status (Prior to Commercial Operation):                            Forecast            Achieved INITIALCRITICALITY INITIALELECTRICITY COtlfM ERCIA L OPER ATION
 
18 OPERATING DATA REPORT DOCKET NO. 50-296 DATE      6-1-80 COi'IPLETED BY TELEPHONE
                                                                                                      ~~~e
                                                                                                        ~~2-            846 OPERATliVG STATUS
: l. Unit Name:      Browns Ferr        - Unit    3                        Notes
: 2. Reporting Period: ~
: 3. Licensed Thermal Power (ilOVt):
: 4. Nameplate Rating (Gross iaaf tVe);
1152
: 5. Design Electrical Rating (Net MWe):
: 6. hfaximum Dependable Capacity (Gross AIWe): 1098-4 7.,faxmi um De p endableCa p acit y (Net iiOVe:)
: 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report. Give Reasons:
N/A
: 9. Power Level To Which Restricted,    If Any (Net ilfWe):
: 10. Reasons For Restrictions, If Any:
This Month            Yr.-to Date         Cumulative
: 11. Hours In Reporting Period                              744                  3 647                28 511
: 12. Number Of Hours Reactor Was Critical                  723.52              3214.95              22122.50
: 13. Reactor Reserve Shutdown Hours                        20.48                20.48              1678.79
: 14. Hours Generator On-Line                              718.45                3186.38            21624.'19
: 15. Unit Reserve Shutdown IIours                          0                    0                    0'3
: 16. Gross Thermal Energy Generated (MWH)                  2 139      84        9 947 427                055 293
: 17. Gross Electrical Energy Generated (MWH)              718 180              3 356 390            20 758 970
: 18. Net Electrical Energy Generated (MPH)                700 399.             3,272,840          20,160,613
: 19. Unit Service Factor
: 20. Unit Availability Factor                                6.6                87.4               75.8
: 21. Unit Capacity Factor (Using i9ifDC Net)               88.4                  84.3                      '6.4 2"". Unit Capacity Factor (Using DER Net)                                       84.3                66.4
: 23. Unit Forced Outage Rate                              3.4                  12.6                9.6
: 24. Shutdowns Scheduled Over iVext 6 Months (Type, Date,and Duration    of Each):
Refuel Outa      e October        1980
: 25. If Shut Down At End Of Report Period. Estimated Date      of Startup:
: 26. Units ln Test Status (Prior,to Commercial Operation):                        Forecast            Achieved IN ITI A L CRITICALIT Y INITIALELECTRICITY COMM ERCIA L OPER ATIOi I (9/77)
 
UNIT SIIUTDOWNS AND POWER REDUCTIONS                    DOCKET NO.           50-259 UNIl NAhIE          Browns Ferr  1 DATE        5-1-80 COhIPLETED BY TELEPI lONE          205-729-6846 4J Licenscc                                    Cause k. Corrective No.            Date                                                                    0  D m  ~lY      Eve>>l                    Q                      Actlotl to Report 4                                    Prevent Rccurrcnce 122          800506            24.44        B                                                      Generator load rejection (No. 6 intermediate valve closed while testin  No. 5    intermediate valve.
123          800507              7.65      A                                                      Turbine trip due to a blown fuse              in "A" feedwater inverter and "B" feedwater hi h level si nal.
124          800523                                                                                Derated  for control rod          sequence exchan e.
125          800527            10.68                                                              Generator load rejection while re-placing  a PK  block in      ma$ n  trans-former creating a differhntial and load re ection ( ersonnel error I
4 F: Forced    ':
Reason:                                                hIethod:                          Exhibit G - Instructions Scheduled        A-Equipment Failure (Explain)                          I -hlanual                        for Preparation of Data B.hlaintenance or Test                                2-h(anual Scram.                  Entry Sheets I'or l.iccnsec C-Refueling                                            3-Aulotnatic Scram.               Evc>>t Rcport (I.ER) File (NURFG-D.Regulatory Restriction                              4.Other (Explain)                  OI 6I )
E.Operator Training 8; Liccnsc Exa>>tination F-Administrative                                                                      5 G-Operational Error (Explain)'I Exl)ibit I - Sr>>>>c Source
"~ '-
(9/77) ~
t              Other (Explain)
 
DOCKET NO.            50-260 UNIT SIIUTDOWNS AND POWER REDUCTIONS UNIT NAhl E        Browns   Ferr 2 DATE o    Cree REPORT  hiON Ill ~Ha                          COhIPLETED BY TELEPI!ONE          205-729-6846 I                                          4J~
Liccnscc        CO41      C                  Cause   & Corrective CP        O Date                            IA r$
CP Event Rcport ¹      v) G        iu Q
0 Aclion to Prevent Rccurrcnce 136      800502        F        20.21      A                                                  To accommodate    repairs to steam leak in steam tunnel.
137      800503        F        14.78      A                                                  To accommodate    repairs to        No. 1 control valve.
138      800509                                                                                  Derated for control rod pattern ad ustment.
139      800516                    8.78      A                                                   To accommodate repairs          to EHC  leak No. 3 servo valve .
I F: Forced              Reason:                                              Method:                          Exhibit G - Instructions S: Scheduled            A.Equipment Failure (Explain)                        I -hlanual                      for Preparation of Data B-hlaintenance or Test                              2.hlanual Scram.                 Entry Sheets fur l.iccnsee C-Refueling                                          3-Automatic Scram.              Event Report (I.L'R) File (NUREG-D.Regulatory Restriction                             4.0llter (Explain)              OI6I)
E.Operator Training& Liccnsc Exanlination
                              ,
F-Administrative
                          ~
G-Opcfattunal Error (Explain)                                                         Exhibit  I - Sante Source (9/77) - i            ~
I I-Other (Explain)
'i ~
 
DOCKET NO.             50-296 UNIT SIIUTDOWNS AND POWER REDUCTIONS                                          Browns Ferr    3 UNIT NAhlE DATE        5-1-80 COhlPLETED IIY TELEPIIONE            205-729-6846 (P
r(      AJ                              Cl Lice nscc  (((        O Cause &. Corrective N((.             Date                      IX
(                Event    IA 'n      Q Q                      A>>lion to J
                                                  ~ (/I        Report ~  cn'Cr      O                    Prevent Rccurrcnce 123          800503                                                                          Derated for maintenance            on  "B" recirculation pump.
124          800515              14.50      G                                                Apparent generator          field    ground-(personnel error).
125          800518                          H                                                Derated for control rod pattern adjustment.
126        , 800521              11.05      B                                                Reactor scrammed while performing reactor low water level SI.
127          800524                                                                          Derated  for control rod pattern adjustment.
128          800530      S                                                                    Derated  for control rod            sequence exchange.,
F: Forced           Reason:                                          hlethod:                           Exhibit G - Instructions I-hlanual                          for Preparation of Data
                ':
Scheduled        A-Equipment Failure (Explain)
B-hlaintenance or Test                           2-hlanual Scram.                  Entry Shc>>ts for l.icensee C-Refueling                                     3-Autonlatic Scraln.              Event Report    (I.l(R) Fil>> (NUREG-D Regulatory Restriction                         4.Other (Explain)                  OI 6 I )
E.Operator Training &. Ucensc Examination F.Adnlinist ra tive G-Operational Error (Explain)'                                                      Exhibit  I - Sa(n>> Source
(()/77)  .              I I Other (Explain)
 
BR011NS,FERRY NUCLEAR PIANT  UNIT    2 CSSC 1:. UIPMFNT                                11ECHANICAL MAINTENANCE SUM 1ARY For the Month of     May      ] 9 80 EFFECT ON SAFE                                                  ACTION TAKEN DATE SYSl~rii      COMPONENT        NATURE OF      OPERATION OF          CAUSE OF              RESULTS OF        TO PRECLUDE MAINTENANCE    THE REACTOR        MALFUNCTION            MALFUNCTION        RECURRENCE 5/15/8  HPCI      Instrument line Instrument  lin        None        Clamps missing      Inoperable instrument Replaced and tightened FE 73-33        sags and clamp                                          line                  clamps missing                                                                      TR 103607
 
WINS    FERRY NUCLEAR PLANT  UNIT CSSC E UIPHENT                          f fECflANICAL MAINTENANCE SUMfARY For the Month of    . Ma/     19 80 EFFECT ON SAFE                                            ACTION TAKEN DATE  SYS'1i;if. COMPONENT  NATURE OF    OPERATION OF            CAUSE OF            RESULTS OF    TO PRECLUDE ffAINTENANCE  THE REACTOR          MALFUNCTION          MALFUNCTION    RECURRENCE 5/15/8  FPC      3A pump     Packing leak          None          Packing leak    Packing leak    Tightened packing TR 182948
 
                                                                                '
BROWNS FERRY NUCLEAR PLANT UNIT CSSC E UIPMENT                             5KQIANICAL MAINTENANCE  


==SUMMARY==
==SUMMARY==
For the Month of DATE SYS'is'.i1 COMPONENT NATURE OF MAINTENANCE EFFECT ON SAFE OPERATION OF THE REACTOR CAUSE OF MALFUNCTION RESULTS OF MALFUNCTION ACTION TAKEN TO PRECLUDE RECURRENCE 5/20/8 HPCI Steam supply drain trap Steam blowing None Gasket leak Bonnet gasket'leak Replaced bonnet gasket TR 103606 5/6/80 HPCI PCV 73-43 Bonnet leak None Bonnet leak Bonnet leak Tightened bonnet bolts TR 165401 CSSC E UIEHENT BROli'HS FERRY NUCLEAR PLANT UNIT 1 ELECTRICAL HAINTENANCE SIMfARY 19 80 D"te 4/30/80 System RHRSW Component 1-B RHRSW Hotor Nature of Haintenance Balance motor after taking initial vibra-tion readings check vibratio after balancin E ecton'ae Operation of The Reactor Cause of Halfunction Hotor out of balance.Results of Halfunction Rendered 1-B RHRSW pump inoperable.
 
Action Taken To Preclude Rocurrence RE-install D3 RHRSW motor.Checked ok.TR8 146733 I5/03/80 Core Spray HCV-75-8 Fuses blowing causing loss of indicating lights.NONE HCV-75-3 wire shorted to side of switch box.Lose light indica-.tions on panel 9-3.Repaired short in switch box.Indi-cating lights check ok.TRP 166327 5/06/80 Radiatio monitoring FCV-1-90-257 FCV-1-90-257 NONE will open but will not make up limit switcl Limit switches burned out FCV-1-90-257 not operating properly.Replaced bad limit u switched.Checked ok.TRf/136942 LER No.259/8040 HROHHR PERRY HUCLEAR PLRHT CHIT ELECTRICAL MAINTENANCE SIMfARY Eor the Month of 19 80 D"te 4/30/80 System RHRSW Component D-3 RHRSW motor Nature of Maintenance Pull D-3 RHRSW motor for re-pair E ecton'a e Operation of The Reactor NONE Cause of Malfunction otor out of balance.Results of Malfunction Rendered D-3 RHRSW pump inoperable.
For the Month of EFFECT ON SAFE                                          ACTION TAKEN DATE SYS'is'.i1   COMPONENT   NATURE OF     OPERATION OF       CAUSE OF         RESULTS OF       TO PRECLUDE MAINTENANCE  THE REACTOR      MALFUNCTION        MALFUNCTION      RECURRENCE 5/20/8   HPCI     Steam supply Steam blowing         None       Gasket leak     Bonnet gasket 'leak Replaced bonnet drain trap                                                                        gasket TR 103606 5/6/80   HPCI     PCV 73-43   Bonnet leak           None       Bonnet leak     Bonnet leak         Tightened bonnet bolts TR 165401
Action Taken To Preclude Recurrence Sent D-3 RHRSW motor to service shop for repair.After repair re-installed motor.Checked ok.TR8 146733, 166926 5/12/80 RCIC EGM Box RCIC operation indicated loss of speed control Unit placed in limiting condi-tion for opera-tion.R9 Diode shorted in EGM box.Loss of speed control.Replaced EGM box.Checked ok per EMI 37.TR8 156718 LER 296/8014.5/25/80 Main Steam Relay 16-AK16 Repair relay 16-AK16 panel 9-43.NONE ontacts arcing nd coil heating po Caused relay 16-AK16 Replaced relay.to malfunction.
 
Checked ok.TR8 143573 CSSC E UIPMENT UROtRIE FERRY NUCLEAR PLANT UNIT I 2&3 INSTRAKNT MAINTENANCE SUI&1ARY FOR THE MONTH OF May 19 8O Unit 1 5-9 SYSTEM Corespray COMPONENT FT-75-49 NATURE OF MAINTENANCE Calibrate EFFECT ON SAFE OPERATION OF THE REACTOR None CAUSE OF MALFUNCTION Instrument Drift RESULTS OF MALFUNCTION Indicated Flow with System Off ACTION.;.TAKEN TO PRECLUDE RECURRENCE None Unit 2 5-8 5 13 RCIC Primary Con tainment FT-71-lA PT-64-138 PDI-64-137 PDI-64-138 Pds-64-137A
BROli'HS FERRY NUCLEAR PLANT UNIT     1 CSSC E UIEHENT                              ELECTRICAL HAINTENANCE SIMfARY 19 80 E  ecton 'ae                                                        Action Taken D"te     System    Component    Nature of      Operation of        Cause of              Results of              To Preclude Haintenance    The Reactor        Halfunction            Halfunction              Rocurrence 4/30/80   RHRSW     1-B RHRSW   Balance motor                     Hotor out of         Rendered 1-B RHRSW     RE-install   D3 RHRSW Hotor      after taking                      balance.              pump  inoperable.      motor. Checked ok.
&B Calibrate Calibrate None None Loss of-Mater Leg Instrument Drift Indicated Flow with System Off Disagreement Between Indicators None None Unit 3 5-.12 Radiation Monitor RM-90-249 Repair None Faulty Ratemeter Card Failed to Calibrate None 5-15 Feedwater LIS-3-56A 6 B Repair None Faulty Switches Failed Surveillance Test None-5-20 5-28 Standby Liquid Con-trol Radwaste LI-53-1B FT-77-16 Maintenance Replace None None Partial Clog of Sensing Line Faulty Transmit te Indication did not Agree with Measure'Probe Transmitter Zero Shift with Pressure None None 28 OUTAGE SlBKARY May 1980 The major emphasis during this reporting period has been on completion of reactor building overhead crane repair, completion of the Unit 3 condenser pull out area radwaste storage zone and work required to effect completion of the security modifications in order to meet the June 30, 1980, NRC commitment dead-line.The final overhead crane wheel bearing inspections are now in progress and should be complete in sufficient time to allow fuel receipt around the middle of June.All work associated with the Unit 3 condenser pull out area radwaste storage zone has been completed, with the exception of painting of floor grating and sump coating.Both of these activities are in progress and will be completed the early part of June.Work on the security modifications is continuing with door multiplexers now being placed in service.The commitment work associated with security should finish on or near June 30.Several other non-outage modifications are in varying stages of completion.
initial vibra-                                                                  TR8 146733 tion readings check vibratio after balancin I5/03/80   Core     HCV-75-8   Fuses blowing     NONE             HCV-75-3   wire       Lose light indica-   Repaired short in Spray                causing loss                        shorted to side    . tions on panel   9-3. switch box. Indi-of indicating                      of switch box.                              cating lights check lights.                                                                        ok. TRP 166327 5/06/80   Radiatio FCV-1-90-257 FCV-1-90-257     NONE             Limit switches       FCV-1-90-257 not       Replaced bad   limit u monitoring              will open but                      burned out            operating properly. switched. Checked will not make                                                                  ok. TRf/ 136942 up limit switcl                                                                LER No. 259/8040
Included in these modifications are installation of safety rails on the condensate storage tanks;installation of guard rails on top of the reactor building elevators; installation of cages around the ladders on the microwave towers;modifications to the RHRSW check valves;installation of H2 and 02 panels and piping for the new Hayes Republic analyzers; installation of snubbers and check valves on plant air compressors; construction of an ambulance storage building;sewage treatment facility modifications; east portal modifications; hypochlorite modifications; condensate storage tank modifications and construction of an outage fabrication shops 29OUTAGE
 
HROHHR PERRY HUCLEAR PLRHT     CHIT ELECTRICAL MAINTENANCE SIMfARY Eor the Month   of                 19 80 E  ecton    'a e                                                      Action Taken D"te     System  Component      Nature of      Operation of          Cause of              Results of            To Preclude Maintenance    The Reactor            Malfunction          Malfunction              Recurrence 4/30/80 RHRSW     D-3 RHRSW     Pull D-3 RHRSW NONE                 otor out of         Rendered D-3 RHRSW Sent D-3 RHRSW motor motor        motor  for re-                      balance.              pump  inoperable. to service shop for pair                                                                            repair. After repair re-installed motor.
Checked ok.
TR8 146733, 166926 5/12/80 RCIC     EGM Box       RCIC operation Unit placed in R9 Diode shorted Loss of speed                 Replaced  EGM box.
indicated loss  limiting condi- in EGM box.             control.              Checked ok per EMI of speed        tion for opera-                                                37. TR8 156718 control          tion.                                                          LER 296/8014.
5/25/80 Main     Relay 16-AK16 Repair relay     NONE                 ontacts arcing     Caused   relay 16-AK16 Replaced relay.
Steam                  16-AK16 panel                        nd coil heating    to malfunction.       Checked ok.
9-43.                                po                                        TR8 143573
 
UROtRIE FERRY NUCLEAR PLANT   UNIT   I 2 & 3 INSTRAKNT MAINTENANCE   SUI &1ARY CSSC E UIPMENT                            FOR THE MONTH OF     May         19   8O NATURE      EFFECT ON SAFE        CAUSE                                  ACTION.;. TAKEN SYSTEM      COMPONENT        OF          OPERATION OF            OF                    RESULTS OF      TO PRECLUDE MAINTENANCE    THE REACTOR        MALFUNCTION              MALFUNCTION      RECURRENCE Unit   1 5-9       Corespray   FT-75-49       Calibrate           None       Instrument   Drift Indicated     Flow with     None System Off Unit   2 5-8       RCIC         FT-71-lA       Calibrate          None        Loss of- Mater Leg      Indicated Flow with      None System Off 5 13      Primary Con  PT-64-138       Calibrate          None        Instrument    Drift    Disagreement Between    None tainment    PDI-64-137                                                             Indicators PDI-64-138 Pds-64-137A &
B Unit   3 5-.12   Radiation   RM-90-249       Repair             None       Faulty Ratemeter       Failed to Calibrate     None Monitor                                                      Card 5-15     Feedwater   LIS-3-56A 6 B Repair             None       Faulty Switches         Failed Surveillance     None Test 20     Standby     LI-53-1B       Maintenance         None       Partial   Clog of       Indication did not       None Liquid Con-                                                  Sensing Line            Agree with Measure trol                                                                                'Probe 5-28    Radwaste    FT-77-16        Replace              None      Faulty Transmit te      Transmitter Zero         None Shift with Pressure
 
28 OUTAGE SlBKARY May 1980 The major emphasis   during this reporting period has been on completion of reactor building overhead crane repair, completion of the Unit           3 condenser pull out area radwaste storage zone and work required to effect completion of the security modifications in order to       meet the June 30, 1980,     NRC commitment dead-line. The final overhead crane wheel bearing inspections are now         in progress and should be complete     in sufficient time to allow fuel receipt       around the middle of June. All work associated with the Unit     3 condenser   pull out   area radwaste storage zone has been completed, with the exception of painting of floor grating and sump   coating. Both of these   activities   are in progress and   will be completed the early part of June.       Work on the   security modifications is continuing with door multiplexers now being placed       in service. The commitment work associated with security should finish       on or near June 30.
Several other non-outage modifications are       in varying stages of completion.
Included in these modifications are       installation of safety rails     on the condensate storage tanks;     installation of   guard rails on top   of the reactor building elevators; installation of     cages around the ladders on the microwave towers;         modifications to the   RHRSW   check valves; installation of H2     and 02 panels and   piping for the new Hayes   Republic analyzers; installation of       snubbers and check valves on     plant air   compressors;   construction of   an ambulance   storage building; sewage treatment facility modifications;     east portal modifications; hypochlorite modifications; condensate   storage tank modifications and construction of an outage fabrication shops
 
29 OUTAGE


==SUMMARY==
==SUMMARY==
(Continued)
(Continued)
May 1980 Work is progressing on schedule on NRC Bulletin 79-14 (hanger inspections) with an estimated 60 percent overall completion.
May 1980 Work is progressing on schedule on NRC Bulletin 79-14 (hanger inspections) with an estimated 60 percent   overall completion.     Anchor repairs associated with NRC Bulletin 79-02 stands at 26 percent complete with 1000 of the iden-tified 3916 anchor repairs being completed.     Research associated with NRC Bulletin 80-08 (fluted head penetration inspection) is essentially complete with a memorandum being prepared   stating results of this inspection.}}
Anchor repairs associated with NRC Bulletin 79-02 stands at 26 percent complete with 1000 of the iden-tified 3916 anchor repairs being completed.
Research associated with NRC Bulletin 80-08 (fluted head penetration inspection) is essentially complete with a memorandum being prepared stating results of this inspection.}}

Revision as of 01:37, 22 October 2019

Monthly Operating Repts for May 1980
ML18025A915
Person / Time
Site: Browns Ferry  Tennessee Valley Authority icon.png
Issue date: 06/01/1980
From:
TENNESSEE VALLEY AUTHORITY
To:
Shared Package
ML18025A912 List:
References
NUDOCS 8006170507
Download: ML18025A915 (32)


Text

TENNESSEE VALLEY AUTHORITY DIVISION OF POWER PRODUCTION BROWNS FERRY NUCLEAR PLANT MONTHLY OPERATING REPORT May 1, 1980 May 31, 1980 DOCKET NRSERS 50-259, 50-260, AND 50-296 LICENSE ~iERS J PR-33, DPR-52, AND DPR-68 Submitted By:

Plant Superintendent 8 0061 V 0503

TABLE OF CONTENTS Operations Summary ~ ~ ~ 1 Refueling Information ~ ~ ~ 4 Significant Operational Events ~ ~ ~ 6 Average Daily Unit Power Level . ~ ~ ~ 13 Operating Data Reports ~ ~ ~ ~ ~ ~ ~ ~ 16 Unit Shutdowns and Power Reductions. ~ ~ e 19 Plant Maintenance ~ ~ ~ 22 Outage Summary 28

0 erations Summar May 1980 The following summary describes the significant operational activities during the reporting period. In support of this summary, a chronological log of significant events is included in this report.

There were fourteen reportable occurrences (plus two supplemental re-ports) reported to the NRC during the month of May.

Unit i There were three scrams on the unit during the month. On May 6, the reactor scrammed due to turbine control valve fast closure from EHC pressure fluctuations. The reactor scrammed on May 7, after the main and RFP turbines tripped from a false high water level signal caused by a blown fuse in the "A" feedwater inverter. On May 27, the reactor scrammed after a generator load rejection caused by the operation of the main transformer differential relay due to personnel error.

Unit 2 There were three scrams on the unit during the month. On May 2, the reactor was manually scrammed to repair a leak on the main steam "B" control valve, second steam leak-off piping flange. The"reactor was manually scrammed on May 3, to repair the EHC servo-valve to the "A" turbine control valve be-cause the servo-valve had been installed incorrectly. On May 16, the reactor was manually scrammed to repair an EHC oil leak in the "C" control valve servo-motor.

0 erations Summar (Continued)

May 1980 Unit 3 There were two scrams on the unit during the month. On May 15, the reactor scrammed due to a generator load rejection when a gr'ound occurred on the gen-erator field ground detector (possible personnel error). The reactor scrammed on May 21, due to high flux on APRM "D" and MSIV "B" and "C" not fully open.

Investigation revealed that the AC pilot valve on the "C" outboard MSIV did not re-energize (defective relay) during tests on the MSL high flow switches.

0 erations Summary (Continued)

Hay 1980 Fati ue Usa e Evaluation The cumulative usage factors for the reactor vessel are as follows:

Location Usa e Factor Unit 1 Unit 2 Unit 3 Shell at water line 0.00464 0.00343 0.00295 Feedwater nozzle 0.21997 0.14835 0.10950 Closure studs 0. 19099 0.12106 0.08794 Note: This accumulated monthly information satisfies technical specification section 6.6.A.17.b(3) reporting requirements.

Common S stems Approximately 9.99E+04 gallons of waste liquid were discharged containing approximately 1.67E-Ol curies of activity.

Refuelin Information May 1980.

Unit 1 Unit 1 is scheduled for its fourth refueling beginning on or about April 15, 1981, with a scheduled restart date of July 25, 1981. This re-fueling will involve loading additional 8 x 8 R (retrofit) fuel assemblies into the core, the final fix on the sparger modification, power supply on LPCI modification, and torus modifications if all approvals are received.

There are 764 fuel assemblies in the reactor vessel. The spent fuel storage pool presently contains 550 spent 7 x 7 fuel assemblies, five 8 x 8 fuel assemblies, one 8 x 8 R fuel assemblies, and 20 new P 8 x 8 R assemblies.

Because of modification work to increase spent fuel pool capacity to 3471 assemblies, present capacity is limited to 1152 assemblies.

Unit 2 Unit 2 is scheduled for its third refueling beginning on or about September 1, 1980, with a scheduled restart date of October 11, 1980.

Resumption of operation on that date will require a change in technical specifications pertaining to the core thermal limits. Li'censing information in support of these changes will be submitted to the NRC before the outage.

This refueling involves replacing some more 7 x 7 fuel assemblies with 8 x 8 R (retrofit) assemblies, and power supply on LPCI modification.

There are 764 fuel assemblies in the reactor vessel. At the end of the month, there were 132 discharged cycle 1 fuel assemblies and 268 discharged cycle 2 fuel assemblies in the spent fuel storage pool. The present storage capacity of the spent fuel pool is 1080 assemblies. With present capacity,

Refuelin Information (Continued)

May 1980 Unit 2 (Continued) the 1979 refueling would be the last refueling that could be discharged to the spent fuel pool without exceeding that capacity and maintaining full core discharge capability in the pool.

Unit 3 Unit 3 is scheduled for its third refueling beginning on or about October 17, 1980, with a scheduled restart date of November 25, 1980. This EOC-3 refueling, involves loading additional 8 x 8 R (retrofit) assemblies into the core, and power supply on LPCX modification.

There are 764 fuel assemblies presently in the reactor vessel. There are 144 discharged cycle 2 fuel assemblies and 208 discharged cycle 1 fuel assemblies in the spent fuel storage pool. The present storage capacity of the spent fuel pool is 1528 assemblies. With present capacity, the 1980 refueling would be the last refueling that could be discharged to the spent fuel pool without exceeding that capacity and maintaining full core discharge capability in the pool.

Si nificant 0 erational Events Unit 1 Date Time Event 5/01/80 0001 Reactor thermal power at 99%, maximum flow (rod limited) sequence "A" 5/02/80 2045 Reduced thermal power from 99% to 95% due to EHC high vibration 2359 Reduced thermal power from 95% to 80% for turbine C.V.

test and SI's 5/03/80 0119 Turbine C.V. tests and SI's completed, commenced power ascension 0230 Reactor thermal power at 95%, holding due to EHC high vibration 5/05/80 1016 Commenced power ascension from 95% thermal power 1402 Reactor thermal power at 99%, maximum flow (rod limited) 5/06/80 0520 Reactor scram No. 124 (2).'rom 99% thermal power on generator load rejection, No. 6 intermediate valve closed while testing No. 5 intermediate valve 5/07/80 0009 Commenced rod withdrawal 0345 Reactor critical No. 144 sequence "A" 0522 Rolled T/G 0546 Synchronized generato~ commenced power ascension 1239 Reactor scram No. 125 from 41% thermal power, turbine trip when fuse blew in "A" feedwater in-verter and "B" feedwater high level tripped turbine and the reactor scrammed 1535 Commenced rod withdrawal 1725 Reactor critical No. 145 sequence "A" 2002 Rolled T/G 2018 Synchronized generator, commenced power ascension 5/08/80 0300 Commenced PCIOHR from 55% thermal power 0530 Reactor thermal power at 72%, holding remote "B" reactor feed pump for maintenance to flow indicator 5/09/80 0450 "B" reactor feed pump maintenance completed and pump placed in service, commenced power ascension 2300 Reactor thermal power at 77%, holding for maintenance to "C" condensate booster pump 5/11/80 0133 "C" condensate booster pump maintenance completed commenced power ascension 0215 Commenced PCIORM from 90% thermal power

Si nificant 0 erational Events Unit 1 Date Time Event 5/11/80 2300 Reactor thermal power at 98% flow limited 5/13/80 1648 Commenced reducing thermal power from 98% due to high EHC vibration 1930 Reactor thermal power at 90%, holding for high EHC vibration 5/15/80 0640 Commenced power ascension 0700 Commenced PCIOMR from 95% thermal power 1315 Reduced thermal power from 98% to 95% due to high EHC vibration 5/16/80 1445 Commenced power ascension 1500 Reactor thermal power at 99%, holding due to high EHC vibration 5/17/80 0339 Reduced thermal power from 99% to 80% for turbine C. V.

tests and SI's 0415 Turbine C. V. tests and SI's completed, commenced power ascension 1500 Reactor thermal power at 99%, holding due to high EHC vibration 5/19/80 1426 Reduced thermal power from 99% to 95% due to high ECH vibration 5/21/80 0730 Commenced power ascension from 95% thermal power 0950 Reactor thermal power at 99%, holding due to high EHC vibration 5/22/80 1500 Reactor thermal power at 99%, holding due to high EHC vibration 5/23/80 2107 Reduced thermal power from 99% to 45% for control rod sequence exchange 2152 Removed "A" recirculation pump M. G. set from service for brush replacement 2209 Reactor thermal power at 45%, commenced control rod se-quence exchange from "A" to "B" 2319 "A" recirculation pump M. G. set brush replacement com-pleted and pump placed in service 2323 "B" recirculation pump M. G.. set removed from service.

for brush replacement 5/24/80 0130 Control rod sequence exchange completed holding for brush replacement on "B" recirculation pump M. G. set 0330 "B" recirculation pump M. G. set brush replacement com-pleted and pump placed in service, commenced power as-cension

Si nificant 0 erational Events Unit 1 Date Time Event 5/25/80 1405 Commenced PCIOMR from 70% thermal power 5/27/80 0845 Reactor thermal power at 98%, holding due to EHC high vibration 2001 Reactor scram No. 126 (1) from 98% thermal power on gen-erator load reject while replacing a PR block in main transformer circuitry creating a differential and load rej ection 5/28/80 0109 Commenced rod withdrawal 0445 Reactor critical No. 146 sequence f lilt 0625 Rolled T/G 0642 Synchronized generator, commenced power ascension 1900 Commenced PCIOMR from 71% thermal power 5/30/80 0030 Reactor thermal power at 97%, EHC vibration limited 5/31/80 2400 Reactor thermal power at 97%, EHC vibration limited

Si nificant 0 erational Events Unit 2 Date Time Event 5/01/80 0001 Reactor thermal power at 98%, CPR limited sequence "A" 2206 Commenced reducing thermal power for shutdown due to steam leak in moisture separator room 5/02/80 0050 Reactor scram No. 98 (manual), from 35% thermal power to accommodate repairs to steam leak 0605 Steam leak fixed, commenced rod withdrawal 1315 Reactor critical No. 109 sequence "B" 2036 Rolled T/G 2102 Synchronized generator, commenced power ascension 5/03/80 0700 Reactor thermal power at 65% holding No. 1 control valve not open 1830 Commenced reducing thermal power for shutdown to correct No. 1 control valve problems 1910 Reactor scram No. 99 (manual) from 35% thermal power to accommodate control valve repairs 5/04/80 0455 No. 1 control valve fixed, commenced rod withdrawal 0624 Reactor critical No. 110 sequence "A" 0938 Rolled T/G 0957 Synchronized generator, commenced power ascension 1900 "Commenced PCIOMR from 70% thermal power 5/05/80 2330 Reactor thermal power at 97%, maximum flow 5/09/80 2225 Reduced thermal power from 97% to 60% for control rod pattern adjustment 5/10/80 0330 Control rod pattern adjustment completed commenced PCIOMR from 60% thermal power 5/12/80 0320 Reactor thermal power at 98%, maximum flow 5/16/80 1805 Commenced decreasing thermal power for shutdown due to EHC leak (No. 3 servo valve) 1840 Reactor scram No. 100 (manual), from 35% thermal power to accommodate EHC maintenance 2135 EHC maintenance completed, commenced rod withdrawal 2330 Reactor critical No. 111 sequence "A" 5/17/80 0301 Rolled T/G 0327 Synchronized generator, commenced power ascension 5/18/80 1440 Commenced PCIOMR from 92% thermal power 5/19/80 0700 Reactor thermal power at 99%, maximum flow 1840 Reduced thermal power from 99% to 90% for removal of "C" string high pressure heaters from service, due to FCV 6-84 flange leak

10 Si nificant 0 erational Events Unit 2 Date Time Event 5/20/80 0450 "C" string high pressure heaters (leak) maintenance completed, commenced power ascension 0530 Commenced PCIOMR from 95% thermal power 2055 Reactor thermal power at 99%, maximum flow 5/24/80 0015 Reduced thermal power from 99% to 80% for turbine C. V. tests and SI's 0220 Turbine C. V. tests and SI's completed 1245 Commenced PCIOMR from 95% thermal power 1500 Reactor thermal power at 99%, maximum flow 5/27/80 0736 Reduced thermal power from 99% to 90% for removal of "C" string high pressure heaters from service for maintenance (leaks) 1443 Maintenance to "C" string high pressures completed and heaters placed in service 1525 Commenced power ascension from 90% thermal power 1630 Commenced PCIOMR from 95% thermal power 1930 Reactor thermal power at 99%, maximum flow 5/31/80 2400 Reactor thermal power at 99%, maximum flow

Si nificant 0 erational Events Unit 3 Date Time Event 5/01/80 0001 Reactor thermal power at 99%, maximum flow (rod limited)

Sequence "A" 5/02/80 0700 Reactor thermal power at 99%, maximum flow (rod limited) 5/03/80 0725 Reduced thermal power from 98% to 50%, tachometer main-tenance on "B" recirculation pump 1440 "B" recirculation pump tachometer maintenance completed and pump placed in service, commenced power ascension 1600 Commenced PCIOMR from 62% thermal power 5/06/80 0030 Reactor thermal power at 99%, maximum flow (rod limited) 5/09/80 2330 Reduced thermal power from 99% to 85% for turbine C. V.

tests and SI's 5/1O/SO 0200 Turbine C. V. tests and SI's completed, commenced PCI(MR from 85% thermal power 0700 Reactor thermal power at 99%, maximum flow 5/15/so o7oo Reduced thermal power from 99% to 70% to perform SI 4.2.A-3 (reactor low y~ter level) 0815 Reactor scram No. 82 , load reject due to generator field ground 1800 Commenced rod withdrawal 2027 Reactor critical No. 92 sequence "A" 2229 Rolled T/G 2245 Synchronized generator, commenced power ascension 5/16/80 0930 Commenced PCIOMR from 65% thermal power 5/18/80 1500 Reactor thermal power at 98%, (rod limited) 2150 Reduced thermal power from 98% to 55% for control rod pattern adjustment 5/19/80 0005 Control rod pattern adjustment completed, commenced power ascension 1800 Commenced PCIOMR from 85% thermal power 5/20/80 2300 Reactor thermal power at 99%, (rod limited) 5/21/80 1348 Reactor scram No. 83 (2) from 99% thermal power while testing of main steam line high flow switches per instruction 4.2.A.7 1944 Commenced rod withdrawal 2205 Reactor critical No. 93 sequence "A" 5/22/80 0031 Rolled T/G 0051 Synchronized generator, commenced power ascension 1630 Commenced PCIOMR from 75% thermal power

Si nificant 0 erational Events Unit 3 Date Time Event 5/23/80 2300 Reactor thermal power at 99%, (rod limited) 5/24/80 2125 Commenced reducing thermal power for control rod pattern adjustment 2235 Reactor thermal power at 55%, holding for control rod pattern adjustment 2335 Removed "A" recirculation pump M.G. set from service for brush replacement 5/25/80 0245 "A" recirculation pump M.G. set brush replacement com-

.pleted and pump placed in service 0252 Removed "B" recirculation pump M.G. set from service for brush replacement 0310 Control rod pattern adjustment completed holding for brush replacement on "B" recirculation pump M.G. set 0415 "B" recirculation pump M.G. set brush replacement and pump placed in service, commenced power ascension 0430 Reactor thermal power at 68%, holding due to "C" main steam line isolation 1315- Commenced power ascension 1830 Commenced PCIOMR from 70% thermal power 5/27/80 0030 Reactor thermal power at 99%, (rod limited) 5/30/80 2200 Reduced thermal power from 99% to 50% for control rod sequence exchange from "A" to "B"

~ 5/31/80 0815 Control rod'equence exchange completed, commenced power ascension 2400 Reactor thermal power at 84%, power ascension in progress (1) Personnel Error (2) Equipment malfunction

13 AVERAGE DAILYUNIT POWER LEVEL DOCKET NO.

UNIT DATE 5-1-80 COMPLETED BY TELEPHONE 205-729-6846 MONTH DAY AVERAGE DAILYPOWER LEVEL DAY AVERAGE DAILYPOWER LEVEL (il(We-Net) (MWe iVet)

I 1064 17 24 1063 18 999 750 19 832 4 835 20 1033 1014 607 21 1071 666 22 1076 23 974 1078 1023 24 1077 25 685 10 1070 957 26 1071 27 1071 1083 1064 28 13 1072 29 1082 1072 1027 14 30 IS 358 31 780 16 703 INSTRUCTIONS Qn this format, list the average daily unit power level in ilDVe.i/et for each day in the reporting month. Compute to the nearest whole megawatt.

(')(77)

14 AVERAGE DAlLYUNIT POWER LEVEL

'I DOCKET NO.

Browns Ferry-1 DATE 5-1-80 COilIPLETED BY Don Green TELEPHONE 205-729-6846 DAY AVERAGE DAlLYPOWER LEVEL DAY AVERAGE DAlLYPOWER LEVEL (i%IWe-Net) (iHWe-Net) 17 1060 1054 18 1026 1014 19 1042 1026 1023 4 20 1037 21 1040 228 1067 22 189 988 23 713 558 799 679 25 10 790 26 879 1008 859 27 12 1042 28 1012 908 13 29 968 1052 30 1005 1031 15 31 16 1047 INSTRUCTIONS On this format, list the average daily unit power level in illWe-Net for each day in the reporting month. Compute to the nearest whole megawatt.

(9 j77)

15 AVERAGE DAILYUNIT POWER LEVEL DOCKET NO.

Browns Ferry-2 DATE COMPLETED BY Don Green TELEPHOiNE MONTH DAY AVERAGE DAILYPOWER LEVEL DAY AVERAGE DAILYPOWER LEVEL (MWe-Net) (MWe-Net) 1 0 560 '7 38 18 913 503 19 1043 4 384 1038 20 954 21 1060 1043 22 1086 1047 1059 23 1043 24 1027 1027 25 1070 10 732'23 26 1058 27 ,1023 1064 1055 12 28 1066 1044 13 29 1061 1039 30 1068 1034 15 31

-16 828 INSTRUCTIONS On this format, list the average daily unit power level in MIVe.Net for each day in the reporting n\onth. Compute to the nearest whole megawatt.

(')(77)

~, ~

16 OPERATING DATA REPORT DOCKET NO ~0-2 DATE 6-1-80 CO41IPLETED BY Green 846 TELEPHONE OPERATING STATUS Browns Ferrv Unit 1 Notes

2. Reporting Period:
3. Licensed Thermal Power (41IWt):
4. Nameplate Rating (Gross 49IWe):
5. Design Electrical Rating (Net 4%We):
6. Maximum Dependable Capacity (Gross 41OVe):
7. Ifavimum De p endableCa p acit y(Net MWe: )
8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons:

N A

9. Power Level To Which Restricted, If Any (Net iWIWe):

IO. Reasons For Restrictions. If Any:

This Month Yr:to-Date Cumuhtive

'

11. Hours In Reporting Period 744 647 51 145
12. Number Of Hours Reactor Was Critical 708.08 1531.68 29808.96
13. Reactor Reserve Shutdown Hours 35.92 283.85 4973.
14. Hours Generator On-Line 701.23 1428.60 29,041.33

~

15. Unit Reserve Shutdown Hours 0 0 0
16. Gross Thermal Energy Generated (MWH) 2,075,263 3,816,795 77,953,288
17. Gross Electrical Energy Generated (MWH) 680 430 2 253 390 25 771 850
18. Net Electrical Energy Generated (MWH) 663,602 1,213,207 25,015,175
19. Unit Service Factor 94.3. 39. 2 56.8
20. Unit Avaihbility Factor 94.3 39. 2 56. 8.
21. Unit Capacity Factor (Using 44IDC Net) 83. 8 31. 2 45.9
22. Unit Capacity Factor (Using DER Net) 83. 8 31. 2 45.9
23. Unit Forced Outage Rate 5.7 18.8 32.4
24. Shutdowns Scheduled Over Next 6 41fonths (Type, Date, and Duration of Each):
25. If Shut Down At End Of Report Period, Estimated Date of Startup:
26. Units In Test Status (Prior to Commercial Operation): Forecast Achieved INITIALCRITICALITY INITIAL ELECTRICITY

~ I COMMERCIAL OPERATION

~ 3 j ~ ~ ,q ~ ,

>~ M

' a i' i." (9/77)

17 OPERATING DATA REPORT 50-260 DOCKET NO.

DATE COtlfPLETED BY

~E}

2'~~

TELEPHONE ~~8-6846 OPERATING STATUS Notes Browns Ferr finest 2

2. Reporting Period:
3. Licensed Thermal Power (MWt):

1152

4. Nameplate Rating (Gross tlfWe):
5. Design Electrical Rating (Net MWe):
6. tlfaximum Dependable Capacity (Gross tbfWe): 1098. 4 7..faxm'um De p e n dable Ca p acit y(Net idWe:) 1065
8. IfChanges Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons:
9. Power Level To Which Restricted, If Any (Net tlfWe):

,"10. Reasons For Restrictions. If Any r

This Month Yr.-to-Date Cumulative

-.11. Hours In Reporting Period 744 3 647 46'0 6

12. Number Of Hours Reactor Was Critical

- 715.52 3 146.60 27 631.08 Reactor Reserve Shutdown Hours 28.48 ~ 12,275.34 13.

14. Hours Geherator On. Line
15. Unit Re~rve Shutdown flours 0 0 0 2 120 551 8 781g400 74 936 400
16. Gross Thermal Energy Generated (MWH) ty. Gross Eteetrieal Energy Generated (ittyH) ~y>> g>O 2 936 690 24 886 758 24 189 526
18. Net Electrical Energy Genersated (MWH)
19. Unit Service Factor 94. 1 84. 1 8.0 Unit'vailability Factor 94. 1 84. 1 58.0 .

'59 20.

21. Unit Capacity Factor (Using tlfDC Net) 87. 6 73.6 49.3
22. Unit Capacity Factor (Using DER Net) 87.6 73.6 49.3
23. Unit Forced Outage Rate 59 35.0
24. Shutdowns Scheduled Over Next 6 Months (Type, Date. and Duration of Each):
25. IfShut Down At End Of Report Period, Estimated Date of Startup:
26. Units In Test Status (Prior to Commercial Operation): Forecast Achieved INITIALCRITICALITY INITIALELECTRICITY COtlfM ERCIA L OPER ATION

18 OPERATING DATA REPORT DOCKET NO. 50-296 DATE 6-1-80 COi'IPLETED BY TELEPHONE

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~~2- 846 OPERATliVG STATUS

l. Unit Name: Browns Ferr - Unit 3 Notes
2. Reporting Period: ~
3. Licensed Thermal Power (ilOVt):
4. Nameplate Rating (Gross iaaf tVe);

1152

5. Design Electrical Rating (Net MWe):
6. hfaximum Dependable Capacity (Gross AIWe): 1098-4 7.,faxmi um De p endableCa p acit y (Net iiOVe:)
8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report. Give Reasons:

N/A

9. Power Level To Which Restricted, If Any (Net ilfWe):
10. Reasons For Restrictions, If Any:

This Month Yr.-to Date Cumulative

11. Hours In Reporting Period 744 3 647 28 511
12. Number Of Hours Reactor Was Critical 723.52 3214.95 22122.50
13. Reactor Reserve Shutdown Hours 20.48 20.48 1678.79
14. Hours Generator On-Line 718.45 3186.38 21624.'19
15. Unit Reserve Shutdown IIours 0 0 0'3
16. Gross Thermal Energy Generated (MWH) 2 139 84 9 947 427 055 293
17. Gross Electrical Energy Generated (MWH) 718 180 3 356 390 20 758 970
18. Net Electrical Energy Generated (MPH) 700 399. 3,272,840 20,160,613
19. Unit Service Factor
20. Unit Availability Factor 6.6 87.4 75.8
21. Unit Capacity Factor (Using i9ifDC Net) 88.4 84.3 '6.4 2"". Unit Capacity Factor (Using DER Net) 84.3 66.4
23. Unit Forced Outage Rate 3.4 12.6 9.6
24. Shutdowns Scheduled Over iVext 6 Months (Type, Date,and Duration of Each):

Refuel Outa e October 1980

25. If Shut Down At End Of Report Period. Estimated Date of Startup:
26. Units ln Test Status (Prior,to Commercial Operation): Forecast Achieved IN ITI A L CRITICALIT Y INITIALELECTRICITY COMM ERCIA L OPER ATIOi I (9/77)

UNIT SIIUTDOWNS AND POWER REDUCTIONS DOCKET NO. 50-259 UNIl NAhIE Browns Ferr 1 DATE 5-1-80 COhIPLETED BY TELEPI lONE 205-729-6846 4J Licenscc Cause k. Corrective No. Date 0 D m ~lY Eve>>l Q Actlotl to Report 4 Prevent Rccurrcnce 122 800506 24.44 B Generator load rejection (No. 6 intermediate valve closed while testin No. 5 intermediate valve.

123 800507 7.65 A Turbine trip due to a blown fuse in "A" feedwater inverter and "B" feedwater hi h level si nal.

124 800523 Derated for control rod sequence exchan e.

125 800527 10.68 Generator load rejection while re-placing a PK block in ma$ n trans-former creating a differhntial and load re ection ( ersonnel error I

4 F: Forced ':

Reason: hIethod: Exhibit G - Instructions Scheduled A-Equipment Failure (Explain) I -hlanual for Preparation of Data B.hlaintenance or Test 2-h(anual Scram. Entry Sheets I'or l.iccnsec C-Refueling 3-Aulotnatic Scram. Evc>>t Rcport (I.ER) File (NURFG-D.Regulatory Restriction 4.Other (Explain) OI 6I )

E.Operator Training 8; Liccnsc Exa>>tination F-Administrative 5 G-Operational Error (Explain)'I Exl)ibit I - Sr>>>>c Source

"~ '-

(9/77) ~

t Other (Explain)

DOCKET NO. 50-260 UNIT SIIUTDOWNS AND POWER REDUCTIONS UNIT NAhl E Browns Ferr 2 DATE o Cree REPORT hiON Ill ~Ha COhIPLETED BY TELEPI!ONE 205-729-6846 I 4J~

Liccnscc CO41 C Cause & Corrective CP O Date IA r$

CP Event Rcport ¹ v) G iu Q

0 Aclion to Prevent Rccurrcnce 136 800502 F 20.21 A To accommodate repairs to steam leak in steam tunnel.

137 800503 F 14.78 A To accommodate repairs to No. 1 control valve.

138 800509 Derated for control rod pattern ad ustment.

139 800516 8.78 A To accommodate repairs to EHC leak No. 3 servo valve .

I F: Forced Reason: Method: Exhibit G - Instructions S: Scheduled A.Equipment Failure (Explain) I -hlanual for Preparation of Data B-hlaintenance or Test 2.hlanual Scram. Entry Sheets fur l.iccnsee C-Refueling 3-Automatic Scram. Event Report (I.L'R) File (NUREG-D.Regulatory Restriction 4.0llter (Explain) OI6I)

E.Operator Training& Liccnsc Exanlination

,

F-Administrative

~

G-Opcfattunal Error (Explain) Exhibit I - Sante Source (9/77) - i ~

I I-Other (Explain)

'i ~

DOCKET NO. 50-296 UNIT SIIUTDOWNS AND POWER REDUCTIONS Browns Ferr 3 UNIT NAhlE DATE 5-1-80 COhlPLETED IIY TELEPIIONE 205-729-6846 (P

r( AJ Cl Lice nscc ((( O Cause &. Corrective N((. Date IX

( Event IA 'n Q Q A>>lion to J

~ (/I Report ~ cn'Cr O Prevent Rccurrcnce 123 800503 Derated for maintenance on "B" recirculation pump.

124 800515 14.50 G Apparent generator field ground-(personnel error).

125 800518 H Derated for control rod pattern adjustment.

126 , 800521 11.05 B Reactor scrammed while performing reactor low water level SI.

127 800524 Derated for control rod pattern adjustment.

128 800530 S Derated for control rod sequence exchange.,

F: Forced Reason: hlethod: Exhibit G - Instructions I-hlanual for Preparation of Data

':

Scheduled A-Equipment Failure (Explain)

B-hlaintenance or Test 2-hlanual Scram. Entry Shc>>ts for l.icensee C-Refueling 3-Autonlatic Scraln. Event Report (I.l(R) Fil>> (NUREG-D Regulatory Restriction 4.Other (Explain) OI 6 I )

E.Operator Training &. Ucensc Examination F.Adnlinist ra tive G-Operational Error (Explain)' Exhibit I - Sa(n>> Source

(()/77) . I I Other (Explain)

BR011NS,FERRY NUCLEAR PIANT UNIT 2 CSSC 1:. UIPMFNT 11ECHANICAL MAINTENANCE SUM 1ARY For the Month of May ] 9 80 EFFECT ON SAFE ACTION TAKEN DATE SYSl~rii COMPONENT NATURE OF OPERATION OF CAUSE OF RESULTS OF TO PRECLUDE MAINTENANCE THE REACTOR MALFUNCTION MALFUNCTION RECURRENCE 5/15/8 HPCI Instrument line Instrument lin None Clamps missing Inoperable instrument Replaced and tightened FE 73-33 sags and clamp line clamps missing TR 103607

WINS FERRY NUCLEAR PLANT UNIT CSSC E UIPHENT f fECflANICAL MAINTENANCE SUMfARY For the Month of . Ma/ 19 80 EFFECT ON SAFE ACTION TAKEN DATE SYS'1i;if. COMPONENT NATURE OF OPERATION OF CAUSE OF RESULTS OF TO PRECLUDE ffAINTENANCE THE REACTOR MALFUNCTION MALFUNCTION RECURRENCE 5/15/8 FPC 3A pump Packing leak None Packing leak Packing leak Tightened packing TR 182948

'

BROWNS FERRY NUCLEAR PLANT UNIT CSSC E UIPMENT 5KQIANICAL MAINTENANCE

SUMMARY

For the Month of EFFECT ON SAFE ACTION TAKEN DATE SYS'is'.i1 COMPONENT NATURE OF OPERATION OF CAUSE OF RESULTS OF TO PRECLUDE MAINTENANCE THE REACTOR MALFUNCTION MALFUNCTION RECURRENCE 5/20/8 HPCI Steam supply Steam blowing None Gasket leak Bonnet gasket 'leak Replaced bonnet drain trap gasket TR 103606 5/6/80 HPCI PCV 73-43 Bonnet leak None Bonnet leak Bonnet leak Tightened bonnet bolts TR 165401

BROli'HS FERRY NUCLEAR PLANT UNIT 1 CSSC E UIEHENT ELECTRICAL HAINTENANCE SIMfARY 19 80 E ecton 'ae Action Taken D"te System Component Nature of Operation of Cause of Results of To Preclude Haintenance The Reactor Halfunction Halfunction Rocurrence 4/30/80 RHRSW 1-B RHRSW Balance motor Hotor out of Rendered 1-B RHRSW RE-install D3 RHRSW Hotor after taking balance. pump inoperable. motor. Checked ok.

initial vibra- TR8 146733 tion readings check vibratio after balancin I5/03/80 Core HCV-75-8 Fuses blowing NONE HCV-75-3 wire Lose light indica- Repaired short in Spray causing loss shorted to side . tions on panel 9-3. switch box. Indi-of indicating of switch box. cating lights check lights. ok. TRP 166327 5/06/80 Radiatio FCV-1-90-257 FCV-1-90-257 NONE Limit switches FCV-1-90-257 not Replaced bad limit u monitoring will open but burned out operating properly. switched. Checked will not make ok. TRf/ 136942 up limit switcl LER No. 259/8040

HROHHR PERRY HUCLEAR PLRHT CHIT ELECTRICAL MAINTENANCE SIMfARY Eor the Month of 19 80 E ecton 'a e Action Taken D"te System Component Nature of Operation of Cause of Results of To Preclude Maintenance The Reactor Malfunction Malfunction Recurrence 4/30/80 RHRSW D-3 RHRSW Pull D-3 RHRSW NONE otor out of Rendered D-3 RHRSW Sent D-3 RHRSW motor motor motor for re- balance. pump inoperable. to service shop for pair repair. After repair re-installed motor.

Checked ok.

TR8 146733, 166926 5/12/80 RCIC EGM Box RCIC operation Unit placed in R9 Diode shorted Loss of speed Replaced EGM box.

indicated loss limiting condi- in EGM box. control. Checked ok per EMI of speed tion for opera- 37. TR8 156718 control tion. LER 296/8014.

5/25/80 Main Relay 16-AK16 Repair relay NONE ontacts arcing Caused relay 16-AK16 Replaced relay.

Steam 16-AK16 panel nd coil heating to malfunction. Checked ok.

9-43. po TR8 143573

UROtRIE FERRY NUCLEAR PLANT UNIT I 2 & 3 INSTRAKNT MAINTENANCE SUI &1ARY CSSC E UIPMENT FOR THE MONTH OF May 19 8O NATURE EFFECT ON SAFE CAUSE ACTION.;. TAKEN SYSTEM COMPONENT OF OPERATION OF OF RESULTS OF TO PRECLUDE MAINTENANCE THE REACTOR MALFUNCTION MALFUNCTION RECURRENCE Unit 1 5-9 Corespray FT-75-49 Calibrate None Instrument Drift Indicated Flow with None System Off Unit 2 5-8 RCIC FT-71-lA Calibrate None Loss of- Mater Leg Indicated Flow with None System Off 5 13 Primary Con PT-64-138 Calibrate None Instrument Drift Disagreement Between None tainment PDI-64-137 Indicators PDI-64-138 Pds-64-137A &

B Unit 3 5-.12 Radiation RM-90-249 Repair None Faulty Ratemeter Failed to Calibrate None Monitor Card 5-15 Feedwater LIS-3-56A 6 B Repair None Faulty Switches Failed Surveillance None Test 20 Standby LI-53-1B Maintenance None Partial Clog of Indication did not None Liquid Con- Sensing Line Agree with Measure trol 'Probe 5-28 Radwaste FT-77-16 Replace None Faulty Transmit te Transmitter Zero None Shift with Pressure

28 OUTAGE SlBKARY May 1980 The major emphasis during this reporting period has been on completion of reactor building overhead crane repair, completion of the Unit 3 condenser pull out area radwaste storage zone and work required to effect completion of the security modifications in order to meet the June 30, 1980, NRC commitment dead-line. The final overhead crane wheel bearing inspections are now in progress and should be complete in sufficient time to allow fuel receipt around the middle of June. All work associated with the Unit 3 condenser pull out area radwaste storage zone has been completed, with the exception of painting of floor grating and sump coating. Both of these activities are in progress and will be completed the early part of June. Work on the security modifications is continuing with door multiplexers now being placed in service. The commitment work associated with security should finish on or near June 30.

Several other non-outage modifications are in varying stages of completion.

Included in these modifications are installation of safety rails on the condensate storage tanks; installation of guard rails on top of the reactor building elevators; installation of cages around the ladders on the microwave towers; modifications to the RHRSW check valves; installation of H2 and 02 panels and piping for the new Hayes Republic analyzers; installation of snubbers and check valves on plant air compressors; construction of an ambulance storage building; sewage treatment facility modifications; east portal modifications; hypochlorite modifications; condensate storage tank modifications and construction of an outage fabrication shops

29 OUTAGE

SUMMARY

(Continued)

May 1980 Work is progressing on schedule on NRC Bulletin 79-14 (hanger inspections) with an estimated 60 percent overall completion. Anchor repairs associated with NRC Bulletin 79-02 stands at 26 percent complete with 1000 of the iden-tified 3916 anchor repairs being completed. Research associated with NRC Bulletin 80-08 (fluted head penetration inspection) is essentially complete with a memorandum being prepared stating results of this inspection.