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Line 3: |
Line 3: |
| | issue date = 06/28/2007 | | | issue date = 06/28/2007 |
| | title = NRC Inspection Report 05000285-06-018, Reply to a Notice of Violation (NOV) EA-07-047 | | | title = NRC Inspection Report 05000285-06-018, Reply to a Notice of Violation (NOV) EA-07-047 |
| | author name = Reinhart J A | | | author name = Reinhart J |
| | author affiliation = Omaha Public Power District | | | author affiliation = Omaha Public Power District |
| | addressee name = | | | addressee name = |
Line 24: |
Line 24: |
| 3. Letter from NRC (B. S. Mallett) to OPPD (R. T. Ridenoure) | | 3. Letter from NRC (B. S. Mallett) to OPPD (R. T. Ridenoure) |
| dated May 29, 2007 (NRC-07-064) | | dated May 29, 2007 (NRC-07-064) |
|
| |
| SUBJECT: NRC Inspection Report 05000285/2006018, Reply to a Notice of Violation (NOV) EA-07-047 In Reference 3, the NRC transmitted a Notice of Violation (NOV) to the Omaha Public Power District (OPPD). The NOV resulted frommaintenance activities on Containment Spray Header Isolatido Valvee HCV-345 "that caused the valve t0.be. installed in the wrong orientatio In the attachment to this letter6iOPPD las proVideda' | | SUBJECT: NRC Inspection Report 05000285/2006018, Reply to a Notice of Violation (NOV) EA-07-047 In Reference 3, the NRC transmitted a Notice of Violation (NOV) to the Omaha Public Power District (OPPD). The NOV resulted frommaintenance activities on Containment Spray Header Isolatido Valvee HCV-345 "that caused the valve t0.be. installed in the wrong orientatio In the attachment to this letter6iOPPD las proVideda' |
| epjly~to~theNOV. | | epjly~to~theNOV. |
|
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Category:Inspection Report
MONTHYEARIR 05000285/20240032024-10-29029 October 2024 NRC Inspection Report 05000285/2024003 IR 05000285/20240022024-08-21021 August 2024 NRC Inspection Report 05000285/2024002 IR 05000285/20240012024-06-0505 June 2024 NRC Inspection Report 05000285/2024001 IR 05000285/20230062023-12-21021 December 2023 NRC Inspection Report 05000285/2023006 IR 05000285/20230052023-11-0202 November 2023 NRC Inspection Room 05000285/2023005 IR 05000285/20230042023-09-13013 September 2023 NRC Inspection Report 05000285/2023-004 IR 05000285/20230032023-07-10010 July 2023 – NRC Inspection Report 05000285/2023003 IR 05000285/20230022023-06-0505 June 2023 NRC Inspection Report 05000285/2023002 IR 05000285/20230012023-02-24024 February 2023 NRC Inspection Report 05000285/2023001 IR 05000285/20220062023-01-0505 January 2023 NRC Inspection Report 05000285/2022-006 IR 05000285/20220052022-10-26026 October 2022 NRC Inspection Report 05000285/2022-005 IR 05000285/20220042022-09-14014 September 2022 NRC Inspection Report 05000285/2022004 IR 05000285/20220032022-06-15015 June 2022 NRC Inspection Report 05000285/2022003 IR 05000285/20220022022-04-28028 April 2022 NRC Inspection Report 050-00285/2022-002 IR 05000285/20220012022-02-25025 February 2022 NRC Inspection Report 050-00285/2022-001 IR 05000285/20210042021-11-18018 November 2021 NRC Inspection Report 050-00285/2021-004 IR 05000285/20210032021-08-11011 August 2021 NRC Inspection Report 050-00285/2021-003 (Public) IR 05000285/20210022021-05-0707 May 2021 NRC Inspection Report 05000285/2021002 IR 05000285/20210012021-02-17017 February 2021 NRC Inspection Report 05000285/2021001 IR 07200054/20204012020-10-29029 October 2020 Independent Spent Fuel Storage Installation Physical Security Requirements for Independent Spent Fuel Storage Installations Inspection Report 07200054/2020401 IR 05000285/20200022020-09-22022 September 2020 NRC Inspection Report 05000285/2020002 IR 05000285/20190052020-03-12012 March 2020 Independent Spent Fuel Storage Installation (ISFSI) - NRC Inspection Report 050-00285/2019-005 and 072-00054/2019-001 IR 05000206/20190042020-02-20020 February 2020 Independent Spent Fuel Storage Installation (ISFSI) - NRC Inspection Report 05000206/2019 004; 05000361/2019 007; 05000362/2019 007; and 07200054/2019-002 IR 05000285/20190042019-11-26026 November 2019 Inspection Report 050-00285/2019-004 IR 05000285/20190032019-09-13013 September 2019 NRC Inspection Report 050-00285/2019-003 IR 05000285/20190022019-07-23023 July 2019 NRC Inspection Report 05000285/2019002 IR 05000285/20194042019-07-11011 July 2019 NRC Security Baseline Inspection Report 05000285/2019404 IR 05000285/20194032019-06-0404 June 2019 NRC Security Baseline Inspection Report 05000285/2019403 IR 05000285/20190012019-02-12012 February 2019 NRC Inspection Report 050-00285/2019-001 IR 05000285/20180042018-11-19019 November 2018 Omaha Public Power District; Fort Calhoun Station - NRC Inspection Report 05000285/2018-004 IR 05000285/20180032018-09-27027 September 2018 NRC Inspection Report 05000285/2018003 IR 05000285/20184102018-05-17017 May 2018 NRC Security Baseline Inspection Report 05000285/2018410 IR 05000285/20184032018-05-17017 May 2018 NRC Physical Security Inspection Report 05000285/2018403 IR 05000285/20180012018-04-13013 April 2018 NRC Inspection Report 05000285/2018001 IR 05000285/20174032018-04-10010 April 2018 Cancellation of NRC Inspection Report 05000285/2017403 IR 05000285/20170112018-02-0101 February 2018 NRC Inspection Report 05000285/2017-011 IR 05000285/20170022017-11-0909 November 2017 NRC Inspection Reports 05000285/2017002 Through 05000285/2017007 IR 05000285/20170122017-11-0808 November 2017 NRC Inspection Report 05000285/2017-012 IR 05000285/20160062017-09-18018 September 2017 NRC Inspection Report 05000285/2016006 IR 05000285/20170092017-08-0404 August 2017 NRC Inspection Report 05000285/2017-009 IR 05000285/20174052017-06-26026 June 2017 NRC Security Inspection Report 05000285/2017405 and NRC Investigation Report 4-2015-030 IR 05000285/20174062017-06-26026 June 2017 NRC Security Baseline Inspection Report 05000285/2017406 IR 05000285/20170102017-06-15015 June 2017 Independent Spent Fuel Storage Installation Inspection Report 05000285/2017010 and 07200054/2017001 IR 05000285/20170012017-05-0808 May 2017 NRC Inspection Report 05000285/2017001 and 05000285/2017008 IR 05000285/20160042017-01-18018 January 2017 NRC Integrated Inspection Report 05000285/2016004 IR 05000285/20165012017-01-17017 January 2017 NRC Emergency Preparedness Annual Inspection Report 05000285/2016501 IR 05000285/20160032016-11-0808 November 2016 NRC Integrated Inspection Report Number 05000285/2016003 IR 05000285/20164042016-10-28028 October 2016 NRC Security Baseline Inspection Report 05000285/2016404 IR 05000285/20160082016-09-22022 September 2016 NRC Evaluations of Changes, Tests, and Experiments and Permanent Plant Modifications Baseline Inspection Report 05000285/2016008 IR 05000285/20160052016-09-12012 September 2016 Errata for Mid-Cycle Assessment Letter for Fort Calhoun Station (Report 05000285/2016005) 2024-08-21
[Table view] Category:Letter
MONTHYEARIR 05000285/20240032024-10-29029 October 2024 NRC Inspection Report 05000285/2024003 LIC-24-0012, Independent Spent Fuel Storage Installation - Response to Proposed Revision to Decommissioning Quality Assurance Plan (DQAP) - Request for Additional Information2024-10-0707 October 2024 Independent Spent Fuel Storage Installation - Response to Proposed Revision to Decommissioning Quality Assurance Plan (DQAP) - Request for Additional Information LIC-24-0011, Independent Spent Fuel Storage Installation - Response to Application for License Amendment Request to Revise the License Termination Plan - Supplemental Information Needed, EPID L-2024-LLA-00952024-10-0202 October 2024 Independent Spent Fuel Storage Installation - Response to Application for License Amendment Request to Revise the License Termination Plan - Supplemental Information Needed, EPID L-2024-LLA-0095 ML24240A1692024-09-18018 September 2024 Cy 2023 Summary of Decommissioning Trust Fund Status ML24243A1042024-09-12012 September 2024 Proposed Revision to the OPPD FCS DQAP - Request for Additional Information (License No. DPR-40, Docket Nos. 50-285, 72-054, and 71-0256) ML24255A0962024-09-12012 September 2024 License Amendment Request to Revise the License Termination Plan - Request Supplemental Information (License No. DPR-40, Docket No. 50-285) IR 05000285/20240022024-08-21021 August 2024 NRC Inspection Report 05000285/2024002 ML24235A0822024-08-10010 August 2024 Response to Fort Calhoun Station, Unit No. 1 - Phase 1 Final Status Survey Report to Support Approved License Termination Plan - Request for Additional Information - Request for Additional Information (EPID L-2024-DFR-0002) July 8, 2024 ML24180A2082024-07-0808 July 2024 Phase 1 Final Status Survey Reports Request for Additional Information Letter ML24183A3222024-07-0808 July 2024 Proposed Revision to the Omaha Public Power District Fort Calhoun Station Decommissioning Quality Assurance Plan - Acceptance Review LIC-24-0007, License Amendment Request (LAR) to Revise License Termination Plan (LTP)2024-06-18018 June 2024 License Amendment Request (LAR) to Revise License Termination Plan (LTP) IR 05000285/20240012024-06-0505 June 2024 NRC Inspection Report 05000285/2024001 ML24151A6482024-06-0303 June 2024 Changes in Reactor Decommissioning Branch Project Management Assignments for Some Decommissioning Facilities LIC-24-0008, Proposed Revision to the Omaha Public Power District (OPPD) Fort Calhoun Station (FCS) Decommissioning Quality Assurance Plan (Dqap), Unit No. 1 and ISFSI2024-05-16016 May 2024 Proposed Revision to the Omaha Public Power District (OPPD) Fort Calhoun Station (FCS) Decommissioning Quality Assurance Plan (Dqap), Unit No. 1 and ISFSI LIC-24-0003, Independent Spent Fuel Storage Installation - Radiological Effluent Release Report and Radiological Environmental Operating Report2024-04-25025 April 2024 Independent Spent Fuel Storage Installation - Radiological Effluent Release Report and Radiological Environmental Operating Report LIC-24-0006, (Fcs), Unit 1, Independent Spent Fuel Storage Installation, Phase 1 Final Status Survey Report to Support Approved License Termination Plan2024-04-17017 April 2024 (Fcs), Unit 1, Independent Spent Fuel Storage Installation, Phase 1 Final Status Survey Report to Support Approved License Termination Plan ML24079A1702024-03-10010 March 2024 ISFSI, Unit 1 - 10 CFR 50.59 Report, Quality Assurance (QA) Program Changes, Technical Specification Basis Changes, 10 CFR 71.106 Quality Assurance Program Approval, Aging Management Review, Commitment Revisions and Revision of Updated Safe LIC-24-0005, Annual Decommissioning Funding / Irradiated Fuel Management Status Report2024-03-0101 March 2024 Annual Decommissioning Funding / Irradiated Fuel Management Status Report LIC-24-0002, Independent Spent Fuel Storage Installation - Submittal of Annual Radioactive Effluent Release Report2024-02-27027 February 2024 Independent Spent Fuel Storage Installation - Submittal of Annual Radioactive Effluent Release Report ML24019A1672024-01-31031 January 2024 Issuance of Amendment to Renewed Facility License to Add License Condition to Include License Termination Plan Requirements IR 05000285/20230062023-12-21021 December 2023 NRC Inspection Report 05000285/2023006 LIC-23-0007, Response to Fort Calhoun, Unit 1 & Independent Spent Fuel Storage Installation Review of License Amendment Request to Add License Condition to Include License Termination Plan Requirements – Request for Additional Information2023-12-0606 December 2023 Response to Fort Calhoun, Unit 1 & Independent Spent Fuel Storage Installation Review of License Amendment Request to Add License Condition to Include License Termination Plan Requirements – Request for Additional Information IR 05000285/20230052023-11-0202 November 2023 NRC Inspection Room 05000285/2023005 ML23276A0042023-09-28028 September 2023 U.S. EPA Response Letter to NRC Letter on Consultation and Finality on Decommissioning and Decontamination of Contaminated Sites MOU - Fort Calhoun Station, Unit 1 – (License No. DPR-40, Docket No. 50-285) IR 05000285/20230042023-09-13013 September 2023 NRC Inspection Report 05000285/2023-004 LIC-23-0005, Response to Fort Calhoun Station, Unit No. 1 - Review of License Amendment Request to Add License Condition to Include License Termination Plan Requirements - 2nd Request for Additional Information (EPID L-2021-LIT-0000) June 2, 20232023-08-24024 August 2023 Response to Fort Calhoun Station, Unit No. 1 - Review of License Amendment Request to Add License Condition to Include License Termination Plan Requirements - 2nd Request for Additional Information (EPID L-2021-LIT-0000) June 2, 2023 ML23234A2412023-08-18018 August 2023 Email - Letter to M Porath Re Ft Calhoun Unit 1 LTP EA Section 7 Informal Consultation Request ML23234A2392023-08-18018 August 2023 Letter to B Harisis Re Ft Calhoun Unit 1 LTP EA State of Nebraska Comment Request.Pdf IR 05000285/20230032023-07-10010 July 2023 – NRC Inspection Report 05000285/2023003 ML23082A2202023-06-26026 June 2023 Consultation on the Decommissioning of the Fort Calhoun Station Unit 1 Pressurized Water Reactor in Fort Calhoun, Nebraska ML23151A0032023-06-0505 June 2023 – Review of License Amendment Request to Add License Condition to Include License Termination Plan Requirements – 2nd Request for Additional Information (EPID L-2021-LIT-0000) June 2, 2023 IR 05000285/20230022023-06-0505 June 2023 NRC Inspection Report 05000285/2023002 LIC-23-0004, (FCS) Radiological Effluent Release Report and Radiological Environmental Operating Report2023-04-20020 April 2023 (FCS) Radiological Effluent Release Report and Radiological Environmental Operating Report LIC-23-0003, Annual Decommissioning Funding / Irradiated Fuel Management Status Report2023-03-15015 March 2023 Annual Decommissioning Funding / Irradiated Fuel Management Status Report LIC-23-0001, Response to Fort Calhoun Station, Unit No. 1 - Review of License Amendment Request to Add License Condition to Include License Termination Plan Requirements - Request for Additional Information2023-02-27027 February 2023 Response to Fort Calhoun Station, Unit No. 1 - Review of License Amendment Request to Add License Condition to Include License Termination Plan Requirements - Request for Additional Information ML22361A1022023-02-24024 February 2023 Reactor Decommissioning Branch Project Management Changes for Some Decommissioning Facilities and Establishment of Backup Project Manager for All Decommissioning Facilities IR 05000285/20230012023-02-24024 February 2023 NRC Inspection Report 05000285/2023001 LIC-23-0002, Independent Spent Fuel Storage Installation, Annual Radioactive Effluent Release Report2023-02-20020 February 2023 Independent Spent Fuel Storage Installation, Annual Radioactive Effluent Release Report ML23020A0462023-01-19019 January 2023 Threatened and Endangered Species List: Nebraska Ecological Services Field Office IR 05000285/20220062023-01-0505 January 2023 NRC Inspection Report 05000285/2022-006 ML22357A0662022-12-30030 December 2022 Technical RAI Submittal Letter on License Amendment Request for Approval of License Termination Plan IR 05000285/20220052022-10-26026 October 2022 NRC Inspection Report 05000285/2022-005 ML22276A1052022-09-30030 September 2022 Conclusion of Consultation Under Section 106 NHPA for Ft. Calhoun Station LTP ML22258A2732022-09-29029 September 2022 Letter to John Swigart, SHPO; Re., Conclusion of Consultation Under Section 106 Hnpa Fort Calhoun Station Unit 1 ML22265A0262022-09-26026 September 2022 U.S. Nuclear Regulatory Commissions Analysis of Omaha Public Power Districts Decommissioning Status Report (License No. DPR-40, Docket No. 50-285) IR 05000285/20220042022-09-14014 September 2022 NRC Inspection Report 05000285/2022004 ML22138A1252022-08-0303 August 2022 Letter to Mr. Timothy Rhodd, Chairperson, Iowa Tribe of Kansas and Nebraska, Re., Ft Calhoun LTP Section 106 ML22138A1222022-08-0303 August 2022 Letter to Mr. John Shotton, Chairman, Otoe-Missouria Tribe of Indians, Oklahoma, Re., Ft Calhoun LTP Section 106 ML22138A1302022-08-0303 August 2022 Letter to Justin Wood, Principal Chief, Sac and Fox Nation, Oklahoma, Re., Ft Calhoun LTP Section 106 ML22214A0922022-08-0303 August 2022 Letter to Stacy Laravie, Thpo, Ponca Tribe of Nebraska, Re., Ft Calhoun LTP Section 106 2024-09-18
[Table view] Category:Licensee Response to Notice of Violation
MONTHYEARLIC-15-0027, Reply to a Notice of Violation (EA-15-020)2015-04-23023 April 2015 Reply to a Notice of Violation (EA-15-020) IR 05000285/20130132014-05-0202 May 2014 Reply to a Notice of Violation 05000285-13-013 LIC-14-0055, Reply to a Notice of Violation 05000285-13-0132014-05-0202 May 2014 Reply to a Notice of Violation 05000285-13-013 IR 05000285/20140022014-04-18018 April 2014 Reply to Notices of Violations 05000285/2014002 LIC-14-0053, Reply to Notices of Violations 05000285/20140022014-04-18018 April 2014 Reply to Notices of Violations 05000285/2014002 IR 05000285/20130112013-04-24024 April 2013 OPPD, Reply to a Notice of Violation, NRC Inspection Report 05000285-13-011, EA-13-043 LIC-13-0028, OPPD, Reply to a Notice of Violation, NRC Inspection Report 05000285-13-011, EA-13-0432013-04-24024 April 2013 OPPD, Reply to a Notice of Violation, NRC Inspection Report 05000285-13-011, EA-13-043 LIC-12-0180, Omaha Public Power District, Reply to a Notice of Violation IR 05000285-12-005, EA-12-1742012-12-13013 December 2012 Omaha Public Power District, Reply to a Notice of Violation IR 05000285-12-005, EA-12-174 LIC-12-0181, NRC Inspection Report 05000285/2012010, Supplemental Response to the Reply to a Notice of Violation (Nov); EA-12-0232012-12-0303 December 2012 NRC Inspection Report 05000285/2012010, Supplemental Response to the Reply to a Notice of Violation (Nov); EA-12-023 LIC-12-0152, Response to Denial of Violation in NRC Inspection Report 05000285/20120022012-11-0606 November 2012 Response to Denial of Violation in NRC Inspection Report 05000285/2012002 LIC-12-0080, Response to NRC Inspection Report 05000285/2012002, EA-2012-0952012-06-11011 June 2012 Response to NRC Inspection Report 05000285/2012002, EA-2012-095 IR 05000285/20120102012-05-24024 May 2012 NRC Inspection Report 05000285/2012010, Reply to a Notice of Violation (Nov); EA-12-023 LIC-12-0051, NRC Inspection Report 05000285/2012010, Reply to a Notice of Violation (Nov); EA-12-0232012-05-24024 May 2012 NRC Inspection Report 05000285/2012010, Reply to a Notice of Violation (Nov); EA-12-023 LIC-12-0041, NRC Inspection Report 05000285/2011006, Reply to a Notice of Violation; EA-12-035 (Revision 0)2012-04-13013 April 2012 NRC Inspection Report 05000285/2011006, Reply to a Notice of Violation; EA-12-035 (Revision 0) LIC-11-0084, Omaha Public Power District - NRC Inspection Report 05000285/2011007, Reply to a Notice of Violation (Nov); EA-11-0252011-08-17017 August 2011 Omaha Public Power District - NRC Inspection Report 05000285/2011007, Reply to a Notice of Violation (Nov); EA-11-025 IR 05000285/20110072011-08-17017 August 2011 Omaha Public Power District - NRC Inspection Report 05000285/2011007, Reply to a Notice of Violation (Nov); EA-11-025 LIC-11-0011, NRC Inspection Report 05000285/2010008, Reply to a Notice of Violation (Nov); EA-10-084 (Revision 1)2011-06-0707 June 2011 NRC Inspection Report 05000285/2010008, Reply to a Notice of Violation (Nov); EA-10-084 (Revision 1) LIC-10-0098, NRC Inspection Report 05000285-10-008, Reply to a Notice of Violation; EA-10-0842010-11-0505 November 2010 NRC Inspection Report 05000285-10-008, Reply to a Notice of Violation; EA-10-084 LIC-09-0066, Ltr. NRC Inspection Report 05000285-09-003, Reply to a Notice of Violation (NOV) EA-09-1742009-09-0202 September 2009 Ltr. NRC Inspection Report 05000285-09-003, Reply to a Notice of Violation (NOV) EA-09-174 LIC-08-0009, NRC Inspection Report 05000285/2007011, Reply to Notice of Violation (NOV) EA-07-194 (Revision 1)2008-02-15015 February 2008 NRC Inspection Report 05000285/2007011, Reply to Notice of Violation (NOV) EA-07-194 (Revision 1) LIC-07-0089, NRC Inspection Report 05000285/2007007, Reply to a Notice of Deviation2007-10-0505 October 2007 NRC Inspection Report 05000285/2007007, Reply to a Notice of Deviation LIC-07-0062, NRC Inspection Report 05000285-06-018, Reply to a Notice of Violation (NOV) EA-07-0472007-06-28028 June 2007 NRC Inspection Report 05000285-06-018, Reply to a Notice of Violation (NOV) EA-07-047 IR 05000285/20070092007-06-15015 June 2007 NRC Inspection Report 05000285/07009, Reply to Notice of Violation (NOV) EA-07-056 LIC-07-0057, NRC Inspection Report 05000285/07009, Reply to Notice of Violation (NOV) EA-07-0562007-06-15015 June 2007 NRC Inspection Report 05000285/07009, Reply to Notice of Violation (NOV) EA-07-056 IR 05000285/20060152006-09-22022 September 2006 NRC Inspection Report 05000285-06-015, Reply to Notice of Violation LIC-06-0107, NRC Inspection Report 05000285-06-015, Reply to Notice of Violation2006-09-22022 September 2006 NRC Inspection Report 05000285-06-015, Reply to Notice of Violation LIC-05-0055, NRC Inspection Report 05000285-05-010, Reply to a Notice of Violation2005-05-12012 May 2005 NRC Inspection Report 05000285-05-010, Reply to a Notice of Violation LIC-04-0109, Status of Actions Regarding NRC IR 05000285-00-001 for the Fort Calhoun Station2004-10-14014 October 2004 Status of Actions Regarding NRC IR 05000285-00-001 for the Fort Calhoun Station LIC-04-0070, Reply to Notice of Violation to Inspection Report 050000285/20040022004-06-11011 June 2004 Reply to Notice of Violation to Inspection Report 050000285/2004002 LIC-03-0076, NRC Inspection Report 50-285/03-09, Reply to a Notice of Violation (NOV)2003-05-20020 May 2003 NRC Inspection Report 50-285/03-09, Reply to a Notice of Violation (NOV) ML0225408832002-08-26026 August 2002 NRC IR 05000285-02-008, Reply to Notice of Violation 2015-04-23
[Table view] |
Text
IIm -Omaha Public Power District 444 South 16th Street Mall Omaha NE 68102-2247 June 28, 2007 LIC-07-0062 U. S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, DC 20555-0001 References:
1.. Doc 4 .50-285 .2. Letter iroin NRC (A. Vegel) to OPPD (R. T. Ridenoure)
dated March 2, 2007 (NRC-07-0020)
3. Letter from NRC (B. S. Mallett) to OPPD (R. T. Ridenoure)
dated May 29, 2007 (NRC-07-064)
SUBJECT: NRC Inspection Report 05000285/2006018, Reply to a Notice of Violation (NOV) EA-07-047 In Reference 3, the NRC transmitted a Notice of Violation (NOV) to the Omaha Public Power District (OPPD). The NOV resulted frommaintenance activities on Containment Spray Header Isolatido Valvee HCV-345 "that caused the valve t0.be. installed in the wrong orientatio In the attachment to this letter6iOPPD las proVideda'
epjly~to~theNOV.
Based on the critenia provided ih7 the NRC Inspection Manual Chapter- 0609, "Significance Determination
'Procels',". -Attachffi2ii
- .n 2,...rP-oces for .Appealing NRC Characterization of Inspection Findings,"f it. appearsý that 'PPD -hs no basis for appeal;.of this NOV since the NRC has documented the basis for their conclusi*Qn While communicafion and interaction between NRC and OPPD on this issue were generally very good, there was a -lapse in communication effectiveness at a critical point in the process.The NRC provided the preliminary assessment of the safety significanc of this finding in Reference 2." The. preliminar safety, sigT.ficance assessmen indicated an increase in core damage frequency (CDF) for internal events of 5.7E-6/year, or '"6 White" for safety significance.
Following receipt of the preliminary assessment, OPPD requested a regulatory conference which was held on' Apnril16,6.200 During preparations for the regulator conference, ý there was significant open cormmunication between OPPD and the NRC. In Reference 2, theNRC clearly identified those areas where OPPD, and NRC agreed,, and those areas where there was disagreemen It waýsr also Clear in Reference 2 that in preparng,.
for. the regulatory conference, OPPD shouldcdonfeentrate.effortSon those areas of disagreement.>, .. ... .....< ...p4odsg Employment with Equal Opportunity.,.
At the regulatory conference, OPPD provided the probabilistic risk assessment (PRA) model for two dominant scenarios previously discussed with the NRC. The safety significance assessment conducted by OPPD determined the event to be 4.2E-7/year, or "Green" for safety significance.
In Reference 3 the NRC disagreed with OPPD and concluded the safety significance as 5.7E-6/year, or "White." Based on Reference 3, it appears that the NRC changed position on some of the initial areas of agreement with OPPD noted in Reference 2. Had OPPD known that the NRC disagreed with the position on those areas, information would have been presented at the regulatory conference to support OPPD's position.OPPD is supportive of NRC's intent that the Reactor Oversight Process (ROP) should be predictable and repeatabl OPPD is considering working with the Nuclear Energy Institute (NEI) to improve the ROP such that similar situations can be avoided in the future.This letter does not regulatory commitment If you should have any-questions, please contact me., e Director ort Calhoun Station JAR/dkg Attachment c: B. S. Mallet, NRC Regional Administrator, Region IV A. B. Wang, NRC Project Manager L. M. Willoughby, NRC Senior Resident Inspector Winston & Strawn LIC-07-0062 Attachment Page 1 REPLY TO A NOTICE OF VIOLATION Omaha Public Power District Docket No. 50-285 Fort Calhoun Station License No. DPR-40 EA-07-047 During an NRC inspection completed on February 13, 2007, a violation of NRC requirements was identifie In accordance with the NRC Enforcement Policy, this violation is listed below: 10 CFR Part 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings," states, in part, that activities affecting quality shall be prescribed by documented in-- on, procedures, or drawings of a -type appropriate to the circumstances ai'd shall be accomplished in accordance with these instructions, procedures, or drawings.Contrary to the above, in May 2005, Fort Calhoun Station personnel accomplished maintenance activities without procedures appropriate to the circumstances.
Specifically, the licensee performed maintenance and post-maintenance activities on Containment Spray Header Isolation Valve HCV-345 using procedures that were not appropriate to the circumstances because the procedures did not require actions to verify the correct orientation of the valve. As a result, the valve was installed in the wrong orientation during maintenance, and post-maintenance testing did not detect the improper reassembly prior to returning the valve to service. This failure caused one train of the Containment Spray system to be inoperable from May 11, 2005 to September 9, 2006.This violation is associated with a White SDP finding.OPPD Response 1. Reason for the Violation On three separate occasions during the 2005 refueling outage, the containment spray header isolation valve, HCV-345, was removed from the system, disassembled, reassembled, and returned to the system. The activities performed during and following the maintenance did not identify the valve internals had been reassembled incorrectly.
Due to the incorrect assembly, when the valve actuator and remote position indication indicated closed, the valve was open. The valve was approximately 80% closed. The valve is known to have been operating correctly prior to the 2005 outage. In November 1990, an air pressure test of the HCV-345 demonstrated that actual valve position matched indicated positio A review of the maintenance records concluded HCV-345 was not removed from the system between 1990 and 200 LIC-07-0062 Attachment Page 2 Technical Specifications requiite the containmnent spray pumps and associated valves to be operabl HCV-345 is associated with the containment spray pumps and is required to function during accident condition The design basis analysis assumes the spray valves will be fully open when necessar A partially open spray valve would not allow the flow rate used in the design basis accident analysi Therefore, HCV-345 was not capable of performing its specified function and was not operable.A root cause analysis of these events was complete As a result, Fort Calhoun Station (FCS) determined that the maintenance procedure allowed flexibility of performing selected portions of the procedure without providing adequate annotation of risk important steps that could impact the final valve alignmen In addition, reliance on the procedure used tý conduct the maintenance without detailed acceptance criteria or verifications to enistni-proper valve operation resulted in a failure of the post maintenance test process to identify the error in assembly of the valve.2. Corrective Steps Taken and Results Achieved The safety related air operated ball and butterfly valves, that are not containment isolation valves, were identifie Any risk important steps that require annotation and second verification were identifie Post maintenance testing was verified to ensure appropriate criteria exists.In addition, the procedure for the inspection and repair of these control valves has been revised to include the following:
1) Manufacturer's index marks were referenced and the directions to add additional match marks during disassembly were removed.2) Specific acceptance criteria on verifying the valve open or closed as part of final reassembly and annotating these steps as post maintenance test steps was included.3) The format of the procedure was changed to allow partial performance, such as packing replacement.
4) Risk important steps (such as verification of valve position, i.e., post maintenance test)were annotated-and the procedure included a second verifier for these steps.In addition, enhancements were made to the training provided to individuals performing maintenance on HCV-345. The steamfitter mechanic training program master plan was revised to include just-in-time, training prior to outages where HCV-345 is going to be disassemble FCS has also acquired a mock-up of the HCV-345 valve for use in training personne LIC-07-0062 Attachment Page 3 3. Corrective Steps That Will Be Taken To Avoid Further Violations Corrective actions to prevent recurrence have been completed as noted above. Further enhancements may be implemented by the corrective action system.4. The Date When Full Compliance Will Be Achieved Fort Calhoun Station is currently in full compliance.