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Category:Letter
MONTHYEARIR 05000285/20240032024-10-29029 October 2024 NRC Inspection Report 05000285/2024003 LIC-24-0012, Independent Spent Fuel Storage Installation - Response to Proposed Revision to Decommissioning Quality Assurance Plan (DQAP) - Request for Additional Information2024-10-0707 October 2024 Independent Spent Fuel Storage Installation - Response to Proposed Revision to Decommissioning Quality Assurance Plan (DQAP) - Request for Additional Information LIC-24-0011, Independent Spent Fuel Storage Installation - Response to Application for License Amendment Request to Revise the License Termination Plan - Supplemental Information Needed, EPID L-2024-LLA-00952024-10-0202 October 2024 Independent Spent Fuel Storage Installation - Response to Application for License Amendment Request to Revise the License Termination Plan - Supplemental Information Needed, EPID L-2024-LLA-0095 ML24240A1692024-09-18018 September 2024 Cy 2023 Summary of Decommissioning Trust Fund Status ML24243A1042024-09-12012 September 2024 Proposed Revision to the OPPD FCS DQAP - Request for Additional Information (License No. DPR-40, Docket Nos. 50-285, 72-054, and 71-0256) ML24255A0962024-09-12012 September 2024 License Amendment Request to Revise the License Termination Plan - Request Supplemental Information (License No. DPR-40, Docket No. 50-285) IR 05000285/20240022024-08-21021 August 2024 NRC Inspection Report 05000285/2024002 ML24235A0822024-08-10010 August 2024 Response to Fort Calhoun Station, Unit No. 1 - Phase 1 Final Status Survey Report to Support Approved License Termination Plan - Request for Additional Information - Request for Additional Information (EPID L-2024-DFR-0002) July 8, 2024 ML24180A2082024-07-0808 July 2024 Phase 1 Final Status Survey Reports Request for Additional Information Letter ML24183A3222024-07-0808 July 2024 Proposed Revision to the Omaha Public Power District Fort Calhoun Station Decommissioning Quality Assurance Plan - Acceptance Review LIC-24-0007, License Amendment Request (LAR) to Revise License Termination Plan (LTP)2024-06-18018 June 2024 License Amendment Request (LAR) to Revise License Termination Plan (LTP) IR 05000285/20240012024-06-0505 June 2024 NRC Inspection Report 05000285/2024001 ML24151A6482024-06-0303 June 2024 Changes in Reactor Decommissioning Branch Project Management Assignments for Some Decommissioning Facilities LIC-24-0008, Proposed Revision to the Omaha Public Power District (OPPD) Fort Calhoun Station (FCS) Decommissioning Quality Assurance Plan (Dqap), Unit No. 1 and ISFSI2024-05-16016 May 2024 Proposed Revision to the Omaha Public Power District (OPPD) Fort Calhoun Station (FCS) Decommissioning Quality Assurance Plan (Dqap), Unit No. 1 and ISFSI LIC-24-0003, Independent Spent Fuel Storage Installation - Radiological Effluent Release Report and Radiological Environmental Operating Report2024-04-25025 April 2024 Independent Spent Fuel Storage Installation - Radiological Effluent Release Report and Radiological Environmental Operating Report LIC-24-0006, (Fcs), Unit 1, Independent Spent Fuel Storage Installation, Phase 1 Final Status Survey Report to Support Approved License Termination Plan2024-04-17017 April 2024 (Fcs), Unit 1, Independent Spent Fuel Storage Installation, Phase 1 Final Status Survey Report to Support Approved License Termination Plan ML24079A1702024-03-10010 March 2024 ISFSI, Unit 1 - 10 CFR 50.59 Report, Quality Assurance (QA) Program Changes, Technical Specification Basis Changes, 10 CFR 71.106 Quality Assurance Program Approval, Aging Management Review, Commitment Revisions and Revision of Updated Safe LIC-24-0005, Annual Decommissioning Funding / Irradiated Fuel Management Status Report2024-03-0101 March 2024 Annual Decommissioning Funding / Irradiated Fuel Management Status Report LIC-24-0002, Independent Spent Fuel Storage Installation - Submittal of Annual Radioactive Effluent Release Report2024-02-27027 February 2024 Independent Spent Fuel Storage Installation - Submittal of Annual Radioactive Effluent Release Report ML24019A1672024-01-31031 January 2024 Issuance of Amendment to Renewed Facility License to Add License Condition to Include License Termination Plan Requirements IR 05000285/20230062023-12-21021 December 2023 NRC Inspection Report 05000285/2023006 LIC-23-0007, Response to Fort Calhoun, Unit 1 & Independent Spent Fuel Storage Installation Review of License Amendment Request to Add License Condition to Include License Termination Plan Requirements – Request for Additional Information2023-12-0606 December 2023 Response to Fort Calhoun, Unit 1 & Independent Spent Fuel Storage Installation Review of License Amendment Request to Add License Condition to Include License Termination Plan Requirements – Request for Additional Information IR 05000285/20230052023-11-0202 November 2023 NRC Inspection Room 05000285/2023005 ML23276A0042023-09-28028 September 2023 U.S. EPA Response Letter to NRC Letter on Consultation and Finality on Decommissioning and Decontamination of Contaminated Sites MOU - Fort Calhoun Station, Unit 1 – (License No. DPR-40, Docket No. 50-285) IR 05000285/20230042023-09-13013 September 2023 NRC Inspection Report 05000285/2023-004 LIC-23-0005, Response to Fort Calhoun Station, Unit No. 1 - Review of License Amendment Request to Add License Condition to Include License Termination Plan Requirements - 2nd Request for Additional Information (EPID L-2021-LIT-0000) June 2, 20232023-08-24024 August 2023 Response to Fort Calhoun Station, Unit No. 1 - Review of License Amendment Request to Add License Condition to Include License Termination Plan Requirements - 2nd Request for Additional Information (EPID L-2021-LIT-0000) June 2, 2023 ML23234A2412023-08-18018 August 2023 Email - Letter to M Porath Re Ft Calhoun Unit 1 LTP EA Section 7 Informal Consultation Request ML23234A2392023-08-18018 August 2023 Letter to B Harisis Re Ft Calhoun Unit 1 LTP EA State of Nebraska Comment Request.Pdf IR 05000285/20230032023-07-10010 July 2023 – NRC Inspection Report 05000285/2023003 ML23082A2202023-06-26026 June 2023 Consultation on the Decommissioning of the Fort Calhoun Station Unit 1 Pressurized Water Reactor in Fort Calhoun, Nebraska ML23151A0032023-06-0505 June 2023 – Review of License Amendment Request to Add License Condition to Include License Termination Plan Requirements – 2nd Request for Additional Information (EPID L-2021-LIT-0000) June 2, 2023 IR 05000285/20230022023-06-0505 June 2023 NRC Inspection Report 05000285/2023002 LIC-23-0004, (FCS) Radiological Effluent Release Report and Radiological Environmental Operating Report2023-04-20020 April 2023 (FCS) Radiological Effluent Release Report and Radiological Environmental Operating Report LIC-23-0003, Annual Decommissioning Funding / Irradiated Fuel Management Status Report2023-03-15015 March 2023 Annual Decommissioning Funding / Irradiated Fuel Management Status Report LIC-23-0001, Response to Fort Calhoun Station, Unit No. 1 - Review of License Amendment Request to Add License Condition to Include License Termination Plan Requirements - Request for Additional Information2023-02-27027 February 2023 Response to Fort Calhoun Station, Unit No. 1 - Review of License Amendment Request to Add License Condition to Include License Termination Plan Requirements - Request for Additional Information ML22361A1022023-02-24024 February 2023 Reactor Decommissioning Branch Project Management Changes for Some Decommissioning Facilities and Establishment of Backup Project Manager for All Decommissioning Facilities IR 05000285/20230012023-02-24024 February 2023 NRC Inspection Report 05000285/2023001 LIC-23-0002, Independent Spent Fuel Storage Installation, Annual Radioactive Effluent Release Report2023-02-20020 February 2023 Independent Spent Fuel Storage Installation, Annual Radioactive Effluent Release Report ML23020A0462023-01-19019 January 2023 Threatened and Endangered Species List: Nebraska Ecological Services Field Office IR 05000285/20220062023-01-0505 January 2023 NRC Inspection Report 05000285/2022-006 ML22357A0662022-12-30030 December 2022 Technical RAI Submittal Letter on License Amendment Request for Approval of License Termination Plan IR 05000285/20220052022-10-26026 October 2022 NRC Inspection Report 05000285/2022-005 ML22276A1052022-09-30030 September 2022 Conclusion of Consultation Under Section 106 NHPA for Ft. Calhoun Station LTP ML22258A2732022-09-29029 September 2022 Letter to John Swigart, SHPO; Re., Conclusion of Consultation Under Section 106 Hnpa Fort Calhoun Station Unit 1 ML22265A0262022-09-26026 September 2022 U.S. Nuclear Regulatory Commissions Analysis of Omaha Public Power Districts Decommissioning Status Report (License No. DPR-40, Docket No. 50-285) IR 05000285/20220042022-09-14014 September 2022 NRC Inspection Report 05000285/2022004 ML22138A1252022-08-0303 August 2022 Letter to Mr. Timothy Rhodd, Chairperson, Iowa Tribe of Kansas and Nebraska, Re., Ft Calhoun LTP Section 106 ML22138A1222022-08-0303 August 2022 Letter to Mr. John Shotton, Chairman, Otoe-Missouria Tribe of Indians, Oklahoma, Re., Ft Calhoun LTP Section 106 ML22138A1302022-08-0303 August 2022 Letter to Justin Wood, Principal Chief, Sac and Fox Nation, Oklahoma, Re., Ft Calhoun LTP Section 106 ML22214A0922022-08-0303 August 2022 Letter to Stacy Laravie, Thpo, Ponca Tribe of Nebraska, Re., Ft Calhoun LTP Section 106 2024-09-18
[Table view] Category:Licensee Response to Notice of Violation
MONTHYEARLIC-15-0027, Reply to a Notice of Violation (EA-15-020)2015-04-23023 April 2015 Reply to a Notice of Violation (EA-15-020) IR 05000285/20130132014-05-0202 May 2014 Reply to a Notice of Violation 05000285-13-013 LIC-14-0055, Reply to a Notice of Violation 05000285-13-0132014-05-0202 May 2014 Reply to a Notice of Violation 05000285-13-013 IR 05000285/20140022014-04-18018 April 2014 Reply to Notices of Violations 05000285/2014002 LIC-14-0053, Reply to Notices of Violations 05000285/20140022014-04-18018 April 2014 Reply to Notices of Violations 05000285/2014002 IR 05000285/20130112013-04-24024 April 2013 OPPD, Reply to a Notice of Violation, NRC Inspection Report 05000285-13-011, EA-13-043 LIC-13-0028, OPPD, Reply to a Notice of Violation, NRC Inspection Report 05000285-13-011, EA-13-0432013-04-24024 April 2013 OPPD, Reply to a Notice of Violation, NRC Inspection Report 05000285-13-011, EA-13-043 LIC-12-0180, Omaha Public Power District, Reply to a Notice of Violation IR 05000285-12-005, EA-12-1742012-12-13013 December 2012 Omaha Public Power District, Reply to a Notice of Violation IR 05000285-12-005, EA-12-174 LIC-12-0181, NRC Inspection Report 05000285/2012010, Supplemental Response to the Reply to a Notice of Violation (Nov); EA-12-0232012-12-0303 December 2012 NRC Inspection Report 05000285/2012010, Supplemental Response to the Reply to a Notice of Violation (Nov); EA-12-023 LIC-12-0152, Response to Denial of Violation in NRC Inspection Report 05000285/20120022012-11-0606 November 2012 Response to Denial of Violation in NRC Inspection Report 05000285/2012002 LIC-12-0080, Response to NRC Inspection Report 05000285/2012002, EA-2012-0952012-06-11011 June 2012 Response to NRC Inspection Report 05000285/2012002, EA-2012-095 IR 05000285/20120102012-05-24024 May 2012 NRC Inspection Report 05000285/2012010, Reply to a Notice of Violation (Nov); EA-12-023 LIC-12-0051, NRC Inspection Report 05000285/2012010, Reply to a Notice of Violation (Nov); EA-12-0232012-05-24024 May 2012 NRC Inspection Report 05000285/2012010, Reply to a Notice of Violation (Nov); EA-12-023 LIC-12-0041, NRC Inspection Report 05000285/2011006, Reply to a Notice of Violation; EA-12-035 (Revision 0)2012-04-13013 April 2012 NRC Inspection Report 05000285/2011006, Reply to a Notice of Violation; EA-12-035 (Revision 0) LIC-11-0084, Omaha Public Power District - NRC Inspection Report 05000285/2011007, Reply to a Notice of Violation (Nov); EA-11-0252011-08-17017 August 2011 Omaha Public Power District - NRC Inspection Report 05000285/2011007, Reply to a Notice of Violation (Nov); EA-11-025 IR 05000285/20110072011-08-17017 August 2011 Omaha Public Power District - NRC Inspection Report 05000285/2011007, Reply to a Notice of Violation (Nov); EA-11-025 LIC-11-0011, NRC Inspection Report 05000285/2010008, Reply to a Notice of Violation (Nov); EA-10-084 (Revision 1)2011-06-0707 June 2011 NRC Inspection Report 05000285/2010008, Reply to a Notice of Violation (Nov); EA-10-084 (Revision 1) LIC-10-0098, NRC Inspection Report 05000285-10-008, Reply to a Notice of Violation; EA-10-0842010-11-0505 November 2010 NRC Inspection Report 05000285-10-008, Reply to a Notice of Violation; EA-10-084 LIC-09-0066, Ltr. NRC Inspection Report 05000285-09-003, Reply to a Notice of Violation (NOV) EA-09-1742009-09-0202 September 2009 Ltr. NRC Inspection Report 05000285-09-003, Reply to a Notice of Violation (NOV) EA-09-174 LIC-08-0009, NRC Inspection Report 05000285/2007011, Reply to Notice of Violation (NOV) EA-07-194 (Revision 1)2008-02-15015 February 2008 NRC Inspection Report 05000285/2007011, Reply to Notice of Violation (NOV) EA-07-194 (Revision 1) LIC-07-0089, NRC Inspection Report 05000285/2007007, Reply to a Notice of Deviation2007-10-0505 October 2007 NRC Inspection Report 05000285/2007007, Reply to a Notice of Deviation LIC-07-0062, NRC Inspection Report 05000285-06-018, Reply to a Notice of Violation (NOV) EA-07-0472007-06-28028 June 2007 NRC Inspection Report 05000285-06-018, Reply to a Notice of Violation (NOV) EA-07-047 IR 05000285/20070092007-06-15015 June 2007 NRC Inspection Report 05000285/07009, Reply to Notice of Violation (NOV) EA-07-056 LIC-07-0057, NRC Inspection Report 05000285/07009, Reply to Notice of Violation (NOV) EA-07-0562007-06-15015 June 2007 NRC Inspection Report 05000285/07009, Reply to Notice of Violation (NOV) EA-07-056 IR 05000285/20060152006-09-22022 September 2006 NRC Inspection Report 05000285-06-015, Reply to Notice of Violation LIC-06-0107, NRC Inspection Report 05000285-06-015, Reply to Notice of Violation2006-09-22022 September 2006 NRC Inspection Report 05000285-06-015, Reply to Notice of Violation LIC-05-0055, NRC Inspection Report 05000285-05-010, Reply to a Notice of Violation2005-05-12012 May 2005 NRC Inspection Report 05000285-05-010, Reply to a Notice of Violation LIC-04-0109, Status of Actions Regarding NRC IR 05000285-00-001 for the Fort Calhoun Station2004-10-14014 October 2004 Status of Actions Regarding NRC IR 05000285-00-001 for the Fort Calhoun Station LIC-04-0070, Reply to Notice of Violation to Inspection Report 050000285/20040022004-06-11011 June 2004 Reply to Notice of Violation to Inspection Report 050000285/2004002 LIC-03-0076, NRC Inspection Report 50-285/03-09, Reply to a Notice of Violation (NOV)2003-05-20020 May 2003 NRC Inspection Report 50-285/03-09, Reply to a Notice of Violation (NOV) ML0225408832002-08-26026 August 2002 NRC IR 05000285-02-008, Reply to Notice of Violation 2015-04-23
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444 South 16 th Street Mall Omaha, NE 68102-2247
LIC-13-0028 April 24, 2013
U.S. Nuclear Regulatory Commission Attn: Document Control Desk
Washington, DC 20555-0001 References: 1. Docket Number 50-285 Letter from NRC (J. A. Clark) to OPPD (D. J. Bannister), "Fort Calhoun - NRC Integrated Inspection Report Number 05000285/2012002," dated May 11, 2012 (NRC-12-0049) (EA-2012-095) (ML12132A395) 3. Letter from OPPD (D. J. Bannister) to NRC (Document Control Desk), "Response to NRC Inspection Report 05000285/2012002, EA-2012- 095," dated June 11, 2012 (LIC-12-0080) (ML12164A431) 4. Letter from NRC (T. M. Blount) to OPPD (Lou Cortopassi), "Denial of Violation in NRC Inspection Report 05000285/2012002," dated September 14, 2012 (NRC-12-0088) (EA-2012-095) (ML12258A293) 5. Letter from OPPD (Lou Cortopassi), "Response to Denial of Violation in NRC Inspection Report 05000285/2012002,' dated November 6, 2012 (LIC-12-0152) (ML12312A109) 6. Letter from NRC (M. Hay) to OPPD (Lou Cortopassi), Fort Calhoun - NRC Inspection Report Number 05000285/2013011 and Notice of Violation," Dated March 11, 2013 (NRC-13-0029) (EA-13-043) (ML13070A399)
SUBJECT: NRC Inspection Report 05000285/2013011, Reply to a Notice of Violation (NOV); EA-13-043 On March 11, 2013, the Nuclear Regulatory Commission (NRC) transmitted Notice of Violation 05000285/2013011-01, "Cont inued Failure to Classify Intake Structure Sluice Gates as Safety Class 3," (EA-13-043) (Reference 6).
Pursuant to 10 CFR 2.201, OPPD acknowled ges the violation occurred and a response to the NOV is provided in the enclosure to this lette Th e regulatory commitment identified in Reference 5 abov e, is restated on the last page of the enclosur U. S. Nuclear Regulatory Commission LlC-13-0028 April 24, 2013 Page 2 If you should have any questions, please contact Terrence W. Simpkin, Manager, Site Regulatory Assurance, at (402) 533-6263. Louis P. Cortopassi Site Vice President and CNO Enclosure LPC/rjr c: A. T. Howell, NRC Regional Administrator, Region IV L. E. Wilkins, NRC Project Manager J. M. Sebrosky, NRC Project Manager J. C. Kirkland, NRC Senior Resident Inspector LIC-13-0028 Enclosure
Page 1 REPLY TO A NOTICE OF VIOLATION Omaha Public Power District (OPPD) Docket No. 50-285 Fort Calhoun Station (FCS) License No. DPR-40
EA-13-043 During a Nuclear Regulatory Commission (NRC) inspection conducted from November 18, 2012 to February 28, 2013, a violation of NRC requirements was identified. The violation is restated below: Title 10 CFR 50, Appendix B, Criterion III, "Design Control," requires, in part that measures shall be established to assure that applicable regulatory requirements and the design basis, as defined in 10 CFR 50.
2, for those struct ures, systems, and components are correctly translated into specifications, drawings, procedures, and instruction Contrary to the above, the licensee failed to establish measures to assure that applicable regulatory requirements and the design basis for those components were correctly translated into specifications , drawings, procedures, and instruction Specifically, the licensee failed to classify the six intake structure exterior sluice gates and their motor operators as Safety Class 3 as defined in the Updated Safety Analysis Report, Appendix N. Background Information As described in the vendor manual, the intake structure sluice gates were designed and manufactured to result in a nearly watertight enclosur The sluice gates are incorporated barriers that: 1. When open, allow river water to fill the wet cells of the intake structure providing a source of water to the circulation and raw water pumps [they are not part of either system], and 2. When closed they are part of the Fort Calhoun Station's passive flood control system. Sluice Gate Licensing Basis Draft Description provided to District in response to an Atomic Energy Commission (AEC) question in 1970:
"For any water levels above 1007.5, the wa ter level inside the intake structure is controlled by positioning the exte rior sluice gates to severely restrict the inflow into the wet wells, along with pumping out at a rate equal to the inflo Because of the wide head variation available, sluice gate and pump settings are self-balancing with reasonable limits" Preliminary Safety Analysis Report (PSAR) and Final Safety Analysis Report (FSAR)
Section 9.8:
LIC-13-0028 Enclosure
Page 2 "For water levels above 1007.5 feet, the wate r level inside the intake structure is controlled by positioning the exte rior sluice gates to restrict the inflow in to the wet wells to match the rate of pumped outflow. Because of the wide head variations possible, the sluice gate and pump settings are automatic self-balancing within reasonable limits." - The underlined language was re moved during the USAR Verification Project in late 199 Updated Safety Analysis Report (U SAR) Section 9.8 (Current): "The water level inside the intake cells can be controlled by pre-positioning the exterior sluice gates (i.e
., before floodwater reaches t he elevation that prevents access to the sluice gate actuators) to severely restrict the inflow into the cells. Intake cell level is then controlled by va rying the raw water pump output to remove the inlet flow. "
OPPD Response 1. Reason for the Violation OPPD initially denied the or iginal violation in Reference 1 and in Reference 2 the NRC stated its reasons why the violation was vali As a result, OPPD attempted to reclassify the sluice gates as Safety Cla ss 3 (SC3). However, they were never designed, procured, or maintained as a SC3 componen Once it was ascertained that reclassification was not possible, O PPD determined that an alternate means for providing cell level control, during times of high river level, was needed in order to provide flood protection for the raw water pump This method of controlling intake cell level was identified to the NRC in Reference 3 and in the public meeting held on March 27, 2013 (U.S. NRC Accession No.ML13101A223). The planned modification was discussed in the public meeting held on April 22, 2013 (U.S. NRC Accession No.ML13093A473). Additionally, the proposed modification would eliminate the need to reclassify the sluice gates as SC Difficulties in the development of the modification lead to significant delays and the eventual issuance of violation EA-13-043. 2. Corrective Steps Taken and the Results Achieved The sluice gates were inspected during the spring of 2012 and are being cycled monthly to verify closure. 3. Corrective Steps That Will be Taken A modification will be installed that will eliminate the need to re-position the intake structure sluice gates during flood levels between 1,010 and 1,014 feet MS OPPD will submit an amendment request in accordance with the requirements of 10 CFR50.59(c)(2) for the modificatio The amendment request is on track to be submitted at the end of May 201 LIC-13-0028 Enclosure
Page 3 4. Date When Full Compliance Will be Achieved Full compliance will be achieved upon final in stallation of the trash rack blowdown backflow modification which will eliminate the need to reclassify the sluice gates as SC3. References: 1. Letter from OPPD (D. Bannister) to NRC (Document Control Desk), "Response to NRC Inspection Report 05000285/2012002, EA-2012-095," dated June 11, 2012 (LIC-12-0080) (ML12164A431) 2. Letter from NRC (T. M. Blount) to OPPD (Lou Cortopassi), "Denial of Violation in NRC Inspection Report 05000285/2012002," dat ed September 14, 2012 (NRC-12-0088) (EA-2012-095) (ML12258A293) 3. Letter from OPPD (Lou Cortopassi), "Response to Denial of Violation in NRC Inspection Report 05000285/2012002,' dated November 6, 2012 (LIC-12-0152) (ML12312A109)
LIC-13-0028 Enclosure
Page 4 Regulatory Commitments Commitment Date AR Number A modification will be installed that will eliminate the need to re-position the intake structure sluice gates during flood levels between 1,010 and 1,014 feet MSL. June 1, 2013 AR 55733