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{{Adams | |||
| number = ML20129F418 | |||
| issue date = 07/23/1991 | |||
| title = Forwards marked-up Copy of Insp Repts 50-424/90-19 & 50/425/90-19,Suppl 1,which Documents Insp Teams Review & Conclusions Re Allegations at Time of Insp Exit Meeting on 900817 | |||
| author name = Reyes L | |||
| author affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) | |||
| addressee name = Vandenburgh C | |||
| addressee affiliation = NRC OFFICE OF NUCLEAR REACTOR REGULATION (NRR) | |||
| docket = 05000424, 05000425 | |||
| license number = | |||
| contact person = | |||
| case reference number = FOIA-94-208 | |||
| document report number = NUDOCS 9610040144 | |||
| package number = ML20129F106 | |||
| document type = INTERNAL OR EXTERNAL MEMORANDUM, MEMORANDUMS-CORRESPONDENCE | |||
| page count = 56 | |||
}} | |||
See also: [[see also::IR 05000424/1990019]] | |||
=Text= | |||
{{#Wiki_filter:_ __ | |||
UNITED STATES | |||
. [pm neo 'o NUCLEAR REGULATCRY COMMISSION | |||
. [ , CE! ION 11 | |||
; y ,P 101 MARIETTA STREET, N.W. | |||
* | |||
, s ATLANTA, GEOR0dA 30323 | |||
'+,..... | |||
JUL 2 31991 | |||
MEMORANN N F0P, Chris A. VanDenburgh, Chief, Reactive Inspection Section 2 | |||
Vendor Inspection Branch | |||
Division of Reactor Inspections and Safeguards | |||
FROM: Luis A. Reyes, Director e | |||
Division of Reactor Projects | |||
SUBJECT: V0GTLE SPECIAL TEAM INSPECTION - ALLEGATION FOLLOWUP TEAM | |||
DRAFT INSPECTION REPORT (INSPECTION REPORT NOS. 50-424/90-XX | |||
AND50-425/90-XX) | |||
This memorandum refers to the special inspection conducted on August 6 | |||
through 17, 1990, at the Vogtle Electric Generating Plant (VEGP). This | |||
' | |||
inspection involved a review of several allegations regarding the safe | |||
operation of VEGP and the review of operational activities generally related | |||
to the allegations. As discussed in the inspection plan, the inspection was | |||
performed by two separate teams--an operational followup and an allegation | |||
, | |||
followup team. | |||
As decided in a meeting held in Nuclear Regulatory Commission (NRC) head- | |||
quarters on September 26, 1990, the allegation followup team's findings and | |||
conclusions was not included in Inspection Report 50-424/90-19; | |||
50-425/90-19. This information was to be withheld pending the completion of | |||
an Office of Investigation review of the allegations and the inspection | |||
team's conclusions. On January 11, 1991, Inspection Report 50-424,425/90-19 | |||
was issued which included the operational followup team findings. The | |||
remaining issues from the allegation followup team were then left in | |||
Inspection Report 90-XX, pending the completion of Ois' review of the | |||
' | |||
allegations. | |||
On July 9,1991, a meeting was held in Region II, with members of Region | |||
II-DRP, 01, and NRR-PD3-2 and Regional management. It was determined to j | |||
, | |||
- | |||
issue the remainder of the 50-424,425/90-19 report, except for the following i | |||
issues: 1) 12.3 Missed Containment Isolation Valve Surveillance; 2) 12.4 | |||
Mode Change With Inoperable Source Range Monitor Nuclear Instrument; 3) 1 | |||
2.7 Reliability of Emergency Diesel Generators and their corresponding parts | |||
to the Notice of Violations. | |||
This memorandum forwards a marked up copy of Inspection Report 50-424, | |||
425!90-19, Supplement 1, which documents the inspection team's review and | |||
conclusions regarding the allegations as of the time of the inspection exit | |||
meeting on August 17, 1990 The report has already been reviewed by the | |||
' | |||
. | |||
Office of Investigation in Region II for information that clight compromise | |||
their on going investigations. The information that was considered | |||
l | |||
pertinent to these investigations will not be included in the issued report. | |||
- | |||
l \ | |||
* | |||
9610040144 960827 l | |||
PDR FOIA ; | |||
COLAPIN94-200 PDR i | |||
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.. .- _ . - . . - . . . . . .- - .. - - _- . - . - - - . - . - . . . _ - - | |||
. _ | |||
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' ! | |||
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:" I | |||
.. | |||
Chris A. VanDenburgh | |||
. | |||
2 JUL 2 31991 l | |||
: | |||
! | |||
i | |||
If you have any questions concerning this issue, please contact P. Skinner ! | |||
at Ext.16299 or S. Vias at Ext.15350. : | |||
; | |||
'i | |||
' | |||
~/ 4 l | |||
' | |||
Luis A. R | |||
! | |||
Enclosures | |||
~1. Draft Notice of Violation i | |||
2. Draft -Inspection Report ' | |||
50-424,425/90-19 Supplement I | |||
cc w/encis: ! | |||
L. Robinson 01. i | |||
D. Hood, NRR, PD3-2~ t | |||
s.445 | |||
&.%nd | |||
t. %e 5 | |||
6. Jul | |||
l | |||
, | |||
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___._._________-___: | |||
. .. _ _ .. - -- - . . . - - - _~. -- - - - - . _ - | |||
; '; | |||
, ioi maasts ta sie<tti. n. | |||
4 ;; e anc.mA.etonc A 3o323 | |||
. | |||
*;' . M%II G; | |||
; 1 | |||
i Docket Nos. 50-424 and 50-425 J | |||
' | |||
; License Nos. NPF-68 and NPF-81 | |||
i | |||
i Georgia Power Company | |||
: ATTN: Nr. W. G. Hairston, III i | |||
' | |||
4 Senior Vice President - . | |||
i | |||
j Nuclear operations q L | |||
) | |||
< | |||
P.O. Box 1295 y ' | |||
) Birmingham, AL 35201 | |||
Gentlemen: | |||
SUBJECT: VOGTLE SPECIAL TEAM INSPECTION AND NOTICE OF VIDIATION | |||
1 (NRC INSPECTION REPORT 3 | |||
NOS. 50-424/90-19 AND | |||
50-425/90-1gg SuppleAw | |||
; This refers to the inspection conducted by an NRC Special p ! | |||
j | |||
! | |||
Inspection Team | |||
included a | |||
on August 6 through 17, 1990.Jr Tne inspem. ion .Ag' | |||
review of activities authorized for your Vogtle | |||
i | |||
facility. At the conclusion of the inspection, thePffindings were | |||
3 | |||
i | |||
i | |||
discussed with those members of your staff identified in the | |||
j | |||
i | |||
enclosed inspection report. }[ | |||
: Areas examined during the inspection are identified in the report. | |||
! Within these areas, the inspection consisted of selective | |||
examinations of procedures and representative records, interviews | |||
j. with personnel, and observation of activities in progress. | |||
. Based on the results of this inspection, certain of your activities | |||
. | |||
appeared to be in violation of NRC requirements, as specified in | |||
j the enclosed Notice of Violation (Notice). i | |||
i | |||
-1^3 *hatthe inspection concluded that the facility was opera | |||
_ | |||
: a safe mann..- Q dance with the requirements perating | |||
l license, we are conc =..:f that there e veral operational ! | |||
: policies and programs whers we ___ - laantified. As part of i | |||
, your response to the ons identified n sed Notice, | |||
: you are a sted to address each of the weaknesses ___A | |||
l ion summary. | |||
! | |||
! You are required to respond to this letter and Notice and should , | |||
follow the instructions specified in the enclosed Notice when ! | |||
preparing your response to the violations. In your response, you 1 | |||
l should document the specific actions taken and any additional | |||
i actions you plan to prevent recurrence. After reviewing your | |||
' | |||
response to this Notice, including your proposed corrective actions | |||
and the results of future inspections, the NRC will determine | |||
; whether further NRC enforcement action is necessary to ensure | |||
compliance with NRC regulatory requirements. . | |||
- | |||
# | |||
. | |||
Q.4 4t g f & LeM-e t % w e.e U An, 491. d* k, & ~? | |||
- | |||
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i | |||
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2 | |||
M II E | |||
coorgio Pov3r CcIpany | |||
' | |||
4 | |||
a | |||
E d!*ionally, you should respond to each of the o esses are | |||
(The | |||
weaknessesMfied within the report. ary.) The response | |||
specifically annotated-in .the InspectioMhe s3gnificance of the weaknesses | |||
. | |||
should address your analysis at these operat tices do not , | |||
and your actions toof non-compliance or reduce the marg n 7:'ev ^ | |||
evolve int | |||
p ant. | |||
. | |||
' | |||
In accordance with section 2.790 of the NRC's " Rules of Practice," | |||
a copy of this letter and its enclosures will be placed in the NRC | |||
Public Document Room. r | |||
The responses directed by this letter and the enclosed | |||
and Budget as required by the Paperwork Reduction Act of 1980, | |||
Pub. L. No. 96. 511. | |||
Should you have any questions concerning this letter, please | |||
4 contact us. | |||
; | |||
sincerely, | |||
0 | |||
> | |||
i | |||
- | |||
> | |||
ne r | |||
' Regional Administrator f | |||
< | |||
, | |||
Region II | |||
. | |||
I | |||
l | |||
: | |||
Enclosures: | |||
1. Notice of Violation | |||
2. Inspection Report 50-424/90-191 l | |||
50-425/90-19 % (pl* * d 1 | |||
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LIMITED DISTRIBUTION - Not For Public Ralesco h, ' | |||
DRAFT - PREDECISIONAL INFORMATION E,N,";,'" , | |||
* | |||
,- | |||
May 9, 1991 P[ %[ | |||
-> . | |||
. | |||
,, | |||
MEMO DUM FOR: Luis A. Reyes, Director g:~ y .i | |||
Division of Reactor Projects fq ',* : ~ | |||
- | |||
Region II .6.'N ', ' ' | |||
FROM: Chris A. VanDenburgh, Chief NY '- " '-4'.:..T.1 + '- | |||
Reactive Inspection Section - 2 [5EF.('-j ,y.. | |||
Vendor Inspection Branch ; | |||
Division of Reactor Inspection and i | |||
' | |||
Safeguards | |||
SUIL7ECT: VOGTLE ECIAL TEAM INSPECTION - ALLEG TION FOLLOWUP TEAM ; | |||
DRAFT SPECTION REPORT (INSPE ION REPORT NOS. ! | |||
50-424/90 x AND 50-425/90-xx) l | |||
This memorandum refer to the special spection conducted on | |||
August 6 through 17, 19 , at the Vogtle lectric Generating Plant . | |||
(VEGP). This inspection nvolved a rev ew of several allegations | |||
regarding the safe operati of VEGP a d the review of operational ; | |||
i | |||
activities generally relate to the legations. As discussed in | |||
the inspection plan, the ins ction was performed by two separate | |||
teams--an operational followup nd n allegation followup team. At | |||
the conclusion of the inspect , all of the inspection team's , | |||
conclusions with respect to the erations and allegation followup l | |||
were discussed with the me s GP's staff identified in the | |||
I | |||
enclosed draft inspection re rt. | |||
As decided in a meeting hel in Nuclea egulatory Commission (NRC) | |||
headquarters on September 26, 1990, the llegation followup team's | |||
findings and conclusio have not bee included in Inspection | |||
Report 424/90-19; 50-4 /90-19. This info ation has been withheld | |||
pending the completi of an office of Inve igation review of the | |||
allegations and the spection team's conclus ns. This memorandum , | |||
' | |||
forwards a draft spection report (50-424/ -xx; 50-425/90-xx) | |||
s | |||
' | |||
which documents e inspection team's revie and conclusions | |||
regarding the a egations as of the time of th inspection exit | |||
meeting on Au t 17, 1990. | |||
. The areas e amined during the inspection are iden fled in the - | |||
inspection eport. As discussed in Inspection Report -424/90-19; | |||
50-425/90 9, the inspection team concluded that the f ility was | |||
, safely rated. However, the inspection identifie several ' | |||
i instan s in which the VEGP was not operated in accordance ith the , | |||
inten of the Technical Specifications. In additio the | |||
: insp ction identified several potential weaknesses i the | |||
' | |||
: | |||
fa lities' operational r licies and practicc.. | |||
i | |||
LIMITED DISTRIBUTION - Not For Public Release i | |||
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LIMITED DISTRIBUTION - Not For Public Release | |||
DRAFT - PREDECISIONAL INFORMATION | |||
i | |||
Lui A. Reyes -2- ' | |||
The ins'pection team's review of the allegations identified severa | |||
additio 1 weaknesses in these operational policies and practice . | |||
These ar identified in the inspection summary of the enci ed , | |||
' | |||
draft insp ction report. | |||
Based on the t artain | |||
activities app,esults eared toof this inspection | |||
be in violationofof theNRC allegations, | |||
require nts, as | |||
specified in t e enclosed draft Notice of Violation (Notice). | |||
These violations re important because they indicate ( a failure | |||
to implement the r cations and | |||
- | |||
administrative proc,equirements | |||
9 dures, and (2) of the | |||
theTechnical | |||
failure to Speci | |||
pr vide accurate | |||
information to the . | |||
As part of the response to the violations /dentified in the | |||
~ | |||
' | |||
enclosed notice, VEGP should also be requeste to address each of | |||
the concerns listed in t e inspection summa . | |||
t | |||
! | |||
! | |||
Enclosures: | |||
1. Draft Notice of Violation | |||
2. Draft Inspection Report 50-434/90-xx; 50-425/90-xx | |||
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BKGrimes | |||
EWBrach | |||
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LIMITED DISTRIBUTION - Not For Public RalGG00 | |||
DRAFT - PREDECISIONAL INFORMATICN | |||
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NRR/DRIS RII/DRP RII/DRP RII/DRP | |||
JWilcox* RAlello* RStarkey* MBranch* | |||
9/ /90 8/31/9 8/31/90 8/31/90 | |||
1 | |||
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RII/DRP RII RS NRR/DLPQ RJI/DRS | |||
I4arner* MThomas* NHuneauller* ylore | |||
9/27/90 /31/90 8/31/90 8/ 1/90 ; | |||
1 | |||
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RII/DRP NRR/DRIS i | |||
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RCarroll* CVanDenburgh ' | |||
8/31/90 9/ /90 l | |||
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* Se previous concurrences | |||
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LIMITED DISTRIBUTION - Not For Public Release | |||
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LIMITED DISTRIBUTION - Not For Public R31easo | |||
DRAFT - PREDECISIONAL INFORMATION | |||
ENCLOSURE 1 ! | |||
, | |||
NOTICE OF VIOIATION | |||
< | |||
l Georgia Power Company Docket Nos. 50-424 and 50-425 | |||
Vogtle Electric Generating Plant License Nos. NPF-68 and NPF-81 l | |||
3 Units 1 and 2 l | |||
' | |||
, | |||
l | |||
l During an NRC inspection conducted on August 6 through 17, 1990, , | |||
violations of NRC requirements were identified. In accordance with l | |||
; the " General Statement of Policy and Procedure for NRC Enforcement i | |||
! Actions," 10 CFR Part 2, Appendix C (1990), the violations are l | |||
! | |||
i | |||
listed below. ' | |||
! | |||
l | |||
l | |||
" | |||
A. 10 CFR Part 50.9, " Completeness and Accuracy of Information," | |||
requires that info mation provided to the NRC by a licensee | |||
: shall be complete and accurate in all material respects. | |||
I Contrary to the above, the licensee provided g separate | |||
curate | |||
, information to the inspection team on 4heee | |||
1 | |||
occasions. Although the information was provided in unsworn, | |||
1 oral statements, the information provided was significant to | |||
the licensing process. The information was provided by | |||
l licensed operators, supervisors and management concerning | |||
i information which was within their specific responsibilities. 1 i | |||
l The d4ve examples were as follows. (50-424/90-eese-95; 50- l | |||
' | |||
! 90-eas-99) li - I'L l | |||
l | |||
' | |||
IV'2- | |||
1. Containment Isolation Valves: During a Unit 2 | |||
surveillance procedure, the unit shift supervisor (USS) | |||
, | |||
' | |||
i | |||
stated, and the operations manager later confirmed, that | |||
' | |||
j the containment isolation valves for the hydrogen monitor | |||
3 system were allowed to be opened without entering the | |||
3 limiting condition for operation (Ico) action | |||
; requirements for Technical specification (Ts) 3.6.3 | |||
because the valves received an automatic isolation | |||
.3 signal. The inspection identified that these containment | |||
] isolation valves were remotely-operated, manual valves | |||
without automatic isolation signals. (Discussed in | |||
: | |||
Section 2.2.1.1 of Inspection Report 50-424/90-19; 50- | |||
425/90-19) | |||
4 2. Snubber Reduction: The operations manager stated that, | |||
! after the second Unit i refueling outage (1R2), the | |||
! | |||
modifications to tt:e snubbers were done in conjunction ! | |||
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LIMITED DISTRIBUTION - Not For Public Release 1 | |||
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3g personnel Accountabiliev: The operations manager stated that | |||
the shift superintendents (SSs) reported directly to the | |||
operations manager and that he personally prepared their | |||
; | |||
; | |||
performance appraisals. The inspection identified that the | |||
sss reported to the unit superintendent (Us), and that the US | |||
1 personally prepared the performance appraisals of the Sss. j | |||
; (Discussed ;,n section 2.Af of this inspection report) | |||
; O , | |||
4 y) Ts 3. 0. 3 Actions: The unit superintendent indicated that | |||
: there were no Operations Department actions which were i | |||
,2 | |||
' | |||
anticipated or required within the first three hours of | |||
entering the action statement of TS 3.0.3. The inspection | |||
identified that the VEGP management policy and stated practice | |||
, | |||
required preparations for a power reduction, including | |||
8 | |||
informing the load dispatcher within the first hour. | |||
: | |||
' (Discussed in section 2.1.1.3 of Inspection Report 50-424/90- | |||
19; 50-425/90-19) | |||
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- LIMITED DISTRIBUTION - Not For Public Rslease | |||
DRAFT - PREDECISIONAL INFORMATION | |||
1 | |||
with preplanned system outages which were required for i | |||
; | |||
other preventive or corrective maintenance or testing. i | |||
inspection identified that few of the snubber | |||
. < | |||
The | |||
: | |||
modifications were done jointly with pre-planned system j | |||
, | |||
i outages. (Discussed in Section 2.1.1.4 of Inspection | |||
Report 50-424/90-19; 50-425/90-19) | |||
' | |||
;. *=14mhl11tyr vrco j | |||
E== v.nq Diesel-Generater (w) | |||
, | |||
.ncorrectly counted the number of starts and failurgot | |||
1 t DGs and incorrectly represented the EDG re ability i | |||
in a on II presentation on April 9, 199 Although t | |||
I the presen ion was not 'ntended to repr sent a specific , | |||
number of su ssful valid test s specified in l | |||
, | |||
Regulatory Guide ( 1.108 and T . 8.1.1.2a, but rather | |||
i | |||
, | |||
to describe the EDG ma nan test program and the EDG | |||
reliability status, the was not informed of the i | |||
C asked for it during ! | |||
j incorrect information il th | |||
i | |||
the inspection. he confirmat of action (CAL) | |||
response and L nsee Event Report (LER -006 were also , | |||
incorrect A cause they were based on t EDG start l | |||
inform fon that was compiled for the VEGP pre ation ! | |||
I | |||
j in e Region II Office. (Discussed in Section 2. f | |||
* | |||
g[ s inspection report) | |||
I | |||
This is a Severity M vel IV violation (Supplement VII). | |||
2 | |||
l B. Technical Specification 6.7.1.a requires that written | |||
j procedures be established or implemented for those activities | |||
' delineated in Appendix A of Regulatory Guide 1.33, Revision 2, | |||
i February 1978. | |||
l Contrary to the above, two examples were identified in which | |||
; the licensee failed to establish or implement the procedures I | |||
: for these required activities as follows: (50-424/90-ac'M? : | |||
50-425/90-asu-49) 19- G | |||
i | |||
19 - 6 | |||
! 1. Administrative Procedure 00150-C, " Deficiency Control," | |||
i- states that a deficiency card must be written if the | |||
i deficiency involves safety-related components which are | |||
to be dispositioned "use-as-is/ repair," or other | |||
conditions involving safety-related components which | |||
- require engineering support or other technical assistance | |||
; to determine if the component is deficient. | |||
d | |||
on August 17, 1990, the NRC identified that a deficiency | |||
card was not written on re'idual heat removal (RHR) pump | |||
' | |||
f1B (a safety-related component) to document the pump's | |||
! LIMITED DISTRIBUTION - Not For Public Release | |||
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DRAFT - PREDECISIONAL INFORMATION | |||
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' degraded conditions which were dispositioned "use-as-is". | |||
(Discussed in Section 2.2 of this inspection report) | |||
i 2. Administrative Procedure 00100-C, " Quality Assurance | |||
; Records Administration," Paragraph 4.1.1.8, specifies | |||
; that quality assurance (QA) records will exh! bit | |||
: necessary and appropriate signatures or initials and | |||
dates. | |||
[ | |||
. | |||
; On August 17, 1990, the NRC identified that the Unit | |||
i Superintendent incorrectly initialed, dated, and signed | |||
i a QA record which voided Temporary Change Procedure (TCP) | |||
1802-C-7-90-1 to Abnormal Operating Procedure 18028-C, | |||
" Loss of Instrument Air," with the date of June 12, 1990, | |||
i in lieu of the actual date (June 15, 1990) on which the | |||
' | |||
document was signed. (Discussed in Section Jdf of this | |||
i inspection report) g.1b | |||
4 | |||
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This is a Severity Level IV violation (Supplement I). ; | |||
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:: C= re. ::, w=n= :. cra.r4 --cI, corr.cu= - | |||
Action," requires measures to be established to ensure tha [ | |||
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onditions adverse to quality are promptly identified f d | |||
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c rected. In the case of significant conditions adve Ne to | |||
! qua , the measures are required to ensure that theguse of | |||
i the co tion is determined and corrective action Jd taken to | |||
i preclude tition. / | |||
, / | |||
ve, two examples were identified in which | |||
Contrary to th | |||
the licensee fa d to determine and adequate | |||
; | |||
: corrective actions preclude repetitl'o/aplement | |||
n as follows: (50- | |||
l 424/90 .ans- et) / ! | |||
i 14 - 14 / | |||
j 1. On August 17,1900, theWC4etermined that the licensee | |||
" | |||
did not identify the foitat and normal use of the 14:0 | |||
. status sheet as one oJA.he causes of the event described | |||
in Licensee Event Report (LER) '90,-004, " Failure To comply | |||
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; With Technical Specification 3.0N< occurs on Entry Into | |||
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Mode 6"; therefore, corrective action was not taken to | |||
preclude repet'ition of the failure to review Ico-required | |||
actions orAremarks which may be on the back side of the | |||
i LCo status sheet. (Discussed in Section '2.4 of this , | |||
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inspect' ion report) i | |||
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1- 2. | |||
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(chnical Specifications 4.8.1.1.3 and 6.8.2 require hat | |||
, | |||
all valid or non-valid EDG failures be reported to th | |||
NRC in a special report within 30 days. In addition, | |||
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DRAFT - PREDECISIONAL INFORMATION | |||
. Operations Procedure 55038-C, " Diesel Start Log," Section | |||
' | |||
. 0, requires that all EDG failures shall be re or(ed to | |||
t RC in a special report. | |||
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On Augu 17, 1990, the NRC ideptified that the | |||
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j corrective a ions taken in response 4o a previous notice | |||
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of violation e inadequate./ Inspection Report 50- | |||
. | |||
424/s7-57 (dated aber Sj A987) previously identified | |||
l a violation of Tech ' al Specification 4.8.1.1.3, in | |||
! that, all EDG failuresmo not reported to the NRC in a | |||
; special report. During a re w of the start records for | |||
i EDG f1B duringA:he period of h 21 through June 14, | |||
i 1990, the NBC' identified that EDG lures had occurred | |||
l which were'not submitted to the NRC in special report. | |||
; In a difion, the NRC identified that Opera ns Procedure | |||
.l 5 8-C provided inadequate guidance to i tify and | |||
: classify EDG failures. (Discussed in Section 2. this | |||
j inspection report) | |||
This is a Severity I4 vel IV violation (Supplement I). | |||
! Pursuant to the provisions of 10 CFR 2.201, Georgia Power Company | |||
is hereby required to submit a written statement or explanation to | |||
Nuclear Regulatory Commission, ATTN: Document Control | |||
, | |||
i the U.S. | |||
Desk, Washington, DC 20555, with a copy to the Regional | |||
Administrator, Region II, and, if applicable, a copy to the NRC | |||
Resident Inspector within 30 days of the date of the letter i | |||
transmitting this Notice Of Viel: tic . (;5tia) . This reply should | |||
be clearly marked as a " Reply to a Notice of Violation" and should | |||
include for each violation: (1) the reason for the violation, or, | |||
if contested, the basis for disputing the violation, (2) the | |||
corrective steps that have been taken and the results achieved, (3) | |||
the corrective steps that will be taken to avoid further | |||
violations, and (4) the date when full compliance will be achieved. | |||
If an adequate reply is not received within the time specified in | |||
this Notice, an order may be issued to show cause why the license | |||
LIMITED DISTRIBUTION - Not For Public Release | |||
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should not be modified, suspended, or revoked, or why such other | |||
action as may be proper should not be taken. Where good cause is | |||
shown, consideration will be given to extending the response time. | |||
, | |||
FOR THE NUCLEAR REGULATORY COMMISSION | |||
l | |||
Stuart D. Ebneter | |||
Regional Administrator | |||
Region II | |||
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Dated at Atlanta, Georgia | |||
(s r ov\ ! | |||
this day of 199p | |||
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LIMITED DISTRIBUTION - Not For Public Release | |||
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LIMITEL LI TRIGUTICN - Gwt Tw. Fuulb A.lacso | |||
- . . ..u.v wa 4vnnu a n s v,vvu 4 vn | |||
R.ePeer | |||
Eid Judu,6 4 | |||
Te w ts | |||
Report No.: 50-424/90-N and 50-425/90-N , $u f pleMe aN I | |||
Licensce: Georgia Power company | |||
P.O. Box 1295 | |||
Birmingham, AL 35201 . | |||
Docket Nos.: 50-424 and 50-425 License Nos.: NPF-68 and NPF-81 | |||
Facility Name: Vogtle Electric Generating Plant, Units 1 and 2 | |||
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Inspection Conducted: August 6-17, 1990 | |||
1 | |||
Team Members: | |||
Ron Aiello - Resident Inspector, Vogtle | |||
Morris Branch - Senior Resident Inspector, Watts Barr . | |||
' | |||
Robert E. Carroll, Jr. - Project Engineer, DRP, Region II | |||
Larry Garner - Senior Resident Inspector, Robinson | |||
Neal K. Nuneauller - Licensing Examiner, NRR | |||
Larry L. Robinson - Investigator, 01, Region II | |||
Robert D. Starkey - Resident Inspector, Vogtle | |||
Craig T. Tate - Investigator, 01, Region II | |||
Peter A. Taylor - Reactor Inspector, DRS, Region II | |||
McKenzie Thomas - Reactor Inspector, DRS, Region II | |||
' John D. Wilcox, Jr. - Operations Engineer, NRR | |||
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' Team Leader:,. _ _ __. _ _ -- | |||
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" Chfis E Va'nDenburgh, SectTon C'hief | |||
Division of Reactor Inspections and Safeguards | |||
! Office of Nuclear Reactor Regulation | |||
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Appeeved by: _ . | |||
- - ::,re e:r r.y.5g,a q | |||
a s . ten m< =~e m. --3 =t a - gg jg i | |||
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DRAFT - PREDECISIONAL INFORMATION | |||
TABLE OF CONTENTS | |||
suf Wf | |||
g 90, | |||
INSPECTION SUMMARY........................................ -t" | |||
1.0 INS PECTION OBJ ECTIVES . . . . . . . . . . . . . . . . . . . . . . . . . ..... T' | |||
2.0 ALLEGATION FOLLOWUP.................................. Ar | |||
2.1 Improper Installation of FAVA System............ 9- | |||
2.2 Operability of Residual Heat Removal Pump....... 41- | |||
2.3 Mi.e.d -Ce..teinsent Isc1; tion '!;1v; Ourveillance. 10 | |||
2.4 Msde Cheng; "'ith In:perable Source Rang? | |||
3 -Moni te r Ne:l e r ! n t re :n t . . . . . . . . . . . . . . . . . . . . . . 10- | |||
2 .JF Backdating o f Signatures. . . . . . . . . . . . . . . . . . . . . . . . jkP | |||
2.sr Reportability of Previous Engineered Safety | |||
Y Features Actuation System Load Sequencer | |||
Outages......................................... 24' | |||
3.' Reliability cf Esergency Olcsci Cenereters. . . . . . 2- | |||
2.,r Air Quality of Emergency Diesel Generator | |||
6 Starting Air System............................. 34F | |||
2.F b Reportability of Previous System Outages........ 25' | |||
'2..'7 .240 Intimidation of Plant Review Board Members. . . . . . 33- | |||
2 b L kT Personnel Accountability........................ ,3&- | |||
3.0 EXIT INTERVIEWS...................................... )4P | |||
APPENDIX 1 - LIST OF TRANSCRIBED INTERVIEWS. . . . . . . . . . . . . . . JFr | |||
APPENDIX 2 - PERSONS CONTACT 2D. . . . . . . . . . . . . . . . . . . . . . . . . . . . J1r | |||
APPENDIX 3 - LIST OF ACRONYMS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . ,$8'' | |||
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DRAFT - PREDECISIONAL INFORMATION | |||
INSPECTION SUMMARY | |||
Recent activities which have occurred at the Vogtle Electric | |||
Generating Plant (VEGP) have raised concerns within the Nuclear | |||
Regulatory Commission (NRC) as to the ability and the deterinination | |||
of the licensee to operate the facility in a safe and conservative | |||
manner. To address this concern, the NRC performed a special team | |||
inspection to deter 1mine if the licensee operates the facility in | |||
accordance with approved procedures and within the requirements and , | |||
intent of the facility's operating license. In addition to the ! | |||
occurrence of specific events, NRC concerns regarding the safe | |||
operation of the facility were heightened with the receipt of | |||
several allegations relating to operational activities at VEGP. | |||
The aggregation of the facts and circumstances associated with the | |||
operational events and the allegations was viewed as a possible | |||
indicator of a non-conservative attitude on the part of the | |||
facility's operating staff which warranted the immediate initiation I | |||
of special inspection activities. | |||
Specifically, the inspection objectives were to: | |||
1) Assess the operational philosophy, policy, procedures and I | |||
practices of the f acility's operating staff and management I | |||
' | |||
regarding operational safety. | |||
2) Determine the technical validity and safety significance of | |||
::d cf the allegations and their impact on the safe and { | |||
conservative operation of the facility. | |||
These inspection objectives were accomplished by the use of two | |||
inspection teams--an operations followup team and an allegations | |||
followup team. The offorts of these two inspection teams were | |||
closely coordinated; however, they independently pursued the | |||
objectives outlined above. | |||
The operations followup team monitored control room activities on | |||
a 24-hour basis in order to: (1) evaluate the operational | |||
philosophy, policies, procedures, and practices of the operating | |||
. staff and management and (2) determine if the plant was being | |||
i operated in a safe and conservative manner in accordance with the | |||
l facilities' operating license. | |||
! | |||
; The allegations followup team verified the technical validity and | |||
safety significance of each ef the allegations. In addition, with k | |||
the assistance of the OI staff, this team interviewed * members of | |||
4 the plant staff in order to determine (1) their personal | |||
j involvement and knowledge of the specific allegations and (2) their | |||
; practice and understanding of the station operational policies. | |||
3 | |||
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j DRAFT - PREDECISIONAL INFORMATION | |||
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! These-interviews were transcribed. Although an OI investigator was l | |||
l assigned to the inspection team to assist during the transcribed ! | |||
1 interviews, this inspection was not an investigation into th g | |||
! intent of the alleaed violations. Nu muesrep.a5 **t M *M } | |||
, | |||
w (:iewen. e<mo not iunst. | |||
The inspection substantiated the occurrence of the specific events | |||
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described in the allegations. These events resulted i t | |||
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examples o v, lations of regulatory requirements (50-424/90- D l | |||
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50-425/90- )2' "" G/^; .. ;^ ; and two of the events were . | |||
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! previously identified as non-cited violations (50-424/90-10-03 and d | |||
50-425/90-01-01). ::: : : , the ine;rrtier did net rubettntirt | |||
-th:t th: : ::t: :' vielstien vere-perfe n f rith the full- | |||
l | |||
j L,wledge of 'J::Or ::n:; ::nt. Sie cerclerier See herM rper : | |||
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' ;vice Of the lic:::ee's recorde ^^d the Svern testisery ef the | |||
j pe;ple inv;17;d in th: ev::t;. | |||
i: | |||
inspection also identified that on several oc | |||
' | |||
s | |||
) naccurate | |||
i respons agers and supervisors verbally su | |||
4 | |||
information to t e ' tion team durin spection. Although l | |||
the inspection team was a out the accuracy of the i | |||
l | |||
J information provided an did n a basis to conclude or l | |||
i suspect th examples were the result o ss disregard , | |||
' | |||
atory requirements or individual wrongdoing. 1 | |||
I | |||
Ioom | |||
*- --- m.' ' b observations and conclusions of the inspection tem #g::o ) | |||
are detailed in Inspection Report | |||
50-424/90-19; 50-425/90-1C | |||
/ | |||
l | |||
addition, the bases for these previous conclusions are summarizedIn ,)#- | |||
4 | |||
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below. | |||
3 Doerational Policies and Practices | |||
i NRC Inspection Report 50-424/90-19; 50-425/90-19 identified several | |||
; examples in which the licensee's operational policies and practices | |||
' | |||
had the potential to adversely affect the operation of the | |||
i facility. llegation followup team's review of the allegations | |||
: identifiedn additional examples in which the licensee's l | |||
l | |||
operational policies and practices had the potential to adversely | |||
affect the safe operation of the facility 1 "^r err;1:- { | |||
I 1) The licensee's method of conducting Plant Review Board (PRB) | |||
, | |||
meetings had the potential for adversely affecting open | |||
i discussions among the PRB members. This concern was based on | |||
i an example in which a PRB voting member felt intimidated and | |||
4 | |||
feared retribution during a PRB meeting because of the | |||
presence of the general manager and the absence of dissenting | |||
~ | |||
opinions in the PRB meeting minutes. Continued licensee | |||
action is necessary to ensure that PRB members freely and | |||
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j DRAFT - PREDECISIONAL . "ORMATION | |||
openly express their technical opinions and safety concerns. | |||
, (Section.2AC) | |||
i Z7 | |||
i 2) The licensee's practice of signing and dating quality | |||
i assurance records was controlled by administrative procedures; | |||
j however, there was a confirmed exasple in which a signature | |||
j was backdated to reflect the actual date of performance. The ' | |||
} backdating of TCP 1802-C-7-90-1 was verified and was l | |||
1 identified as Violation 50-424/90- ' ~6; 50-4 25/90-aus-et . | |||
*O | |||
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(Section 24) i | |||
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l 3) The licensee' practice of not initiating a deficiency card | |||
(DC) during troubleshooting activities involving the | |||
questioned operability of the residual heat removal (RHR) pump | |||
prevented a documented engineering evaluation for either the | |||
nuclear service cooling water (NSCW) outlet leak or the | |||
excessive vibration on the RHR motor. The fal' lure to | |||
, implesent this administrative procedure was identified as .4 | |||
1 Violation 50-4 2 4/90 .xas-@2. (Section 2.2) | |||
si-4 | |||
, | |||
,i, "''; 11::ncer ' | |||
.. :the'' ef 59*= 4 = 4 a0 ==d eaaWal l i a; en,a 4 == af | |||
, completed surveillance procedures was not controlled y | |||
: inistrative procedures. Based on the confusio hich | |||
i resu d in the missed curveillance of the tainment | |||
j' isolatio alves and a review of this methodo additional | |||
3 atter. tion acessary to ensure that thg procedures are | |||
2 | |||
appropriately c ntrolled and used. (Sect' ion 2.3) | |||
; ,9) The licensee's math to denti tive and informational | |||
limiting condition for oper .ns (Iros) on LCO status sheets | |||
allowed continuation o he ~I40 required ac.tions on the | |||
reverse side of the rm. This me , in conjunction with | |||
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the operator's c reed practice of re wing only the front | |||
side of the status sheets, was one of oot causes for | |||
l a non-ci violation (50-424/90-10-03) conc ng a mode | |||
l cha ich occurred with inoperable source ra uclear | |||
; i ruments. The failure to identify this additiona oot | |||
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v.u.. ... la.ni.iii.4 es Vicletie.. 50 4 ?/00 :: ^3. (!::t _ _ | |||
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fW The licensee's method of appraising the performance of the | |||
licensed operators resulted in a potential disincentive for | |||
identifying items which may result in LERs or violations, | |||
j (Section 2 44) l | |||
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l DRAFT - PREDECISIONAL INFORMATION | |||
Accuraev of Information I | |||
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The inspection concluded that during the inspection inaccurate ' | |||
' information was received on several occasions, from responsible | |||
managers and operators on topp:s well within the scope of * a ir | |||
specific responsibility. In 4Manstances the initial infor Cisn ( | |||
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7e | |||
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supplied was clearly incorrect or inadequately researchef th t : | |||
l inspection team concluded that in each of these example: | |||
licensee officials provided inaccurate, unsworn, oral stat cent s | |||
1 | |||
concerning information which concerned topics well within ts.24r : | |||
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responsibilities, | |||
i ho inaccurate information was | |||
: the 4ir;t th::: cases, the { l | |||
In | |||
significant to the inspection process. Specifically, (1) if the | |||
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' containment isolation valves received an automatic closure signalthe v | |||
' if the snubber modifications had been performed in conjunction with | |||
i other preplanned preventive and corrective maintenance, then the ; | |||
voluntary entries into LCO 3.7.8 would not have been required, end- I | |||
. | |||
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p) ii the-WRC-was.. accurately informed .cf.-the-aumber of 15 p ehich 51::: | |||
; | |||
1 and i.ilorse ;' - th: Ere:gency Diesel Cenerator-No. | |||
uwwuu.a dosinii ts d10 h:: ting, ther additiert! tecting rey hr : j | |||
,.... . .,,. is .4- pries to - th: rele::: .. .... ....... _..... .. ::tden l | |||
1etten The inspection team concluded that the failure to provide ! | |||
accurate information was a violation of the requirements of 10 CFR | |||
50.9 concerning accuracy and completeness of information. The | |||
inspection identified Violation 50-424/90- ; 50-425/90-Jsw-99 in | |||
M - ' ~L | |||
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this area and ncted the following examples: | |||
containment Isolation valves: During a Unit 1 surveillance | |||
, | |||
! 1) | |||
procedure, the unit shif t supervisor (USS) stated, and the | |||
; | |||
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operations manager later confirmed, that the containment | |||
isolation valves for the hydrogen monitor system were allowed | |||
to be opened without entering the 140 action requirements for | |||
. | |||
; | |||
i TS 3.6.3 because the talves received an automatic isolation | |||
i signal. The inspection identified that these containment | |||
i isolation valves were remotely-operated, manual valves without | |||
I auta.tatic isolation signals. (Discussed in Section 2.2.1.1 of ' | |||
Inspect Dn Report 50-424/90-19; 50-425/90-19) | |||
2) Snubber Reduction: The operations manager stated that, after | |||
Unit 1 refueling outage IR2, the modifications to the snubbers | |||
were done in conjunction with preplanned system outages which i | |||
were required for other preventive or corrective maintenance | |||
or testing. The inspection identified that few of the snubber | |||
i modifications were done jointly with pre-planned system | |||
' outages. (Discussed in Section 2.1.1.4 of Inspection Report l | |||
50-424/90-19; 50-425/90-19) j | |||
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DRAFT - PREDECISIONAL INFORMATION | |||
Emeraenev Diesel cenerator Reliability: The licensee's met | |||
researching information for Region II prese ion | |||
conc { | |||
ng the reliability of the emergency diesel , erators ! | |||
(EDGs) v nadequate in that there was a 1 of specific l | |||
. guidance conc ng the EDG information d red coupled with I | |||
inadequate resear the EDG starti story. This method l | |||
resulted in providing omplete , therefore, inaccurate | |||
info mation to the NRC. inn lon, the licensee's response i | |||
to the NRC's confi nation ac letter (CAL) was based on | |||
, | |||
this same inadequate earch. In tion, the subsequent i | |||
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Licensee ' Event rt (LER) 90-006 was so inadequately ! | |||
researched. a result of this method of inv ation, the i | |||
NRC was r informed of the correct operability a until j | |||
this pection. (Discussed in section 2.7 of this inspe n | |||
ort) ! | |||
l | |||
34t Personnel Accountability: Theoperationsmanagerstatedthatl ! | |||
the shift superintendents (sss) reported directly to the ' | |||
operations manager and that he personally prepared their i | |||
performance appraisals. The inspection identified that the : | |||
SSs reported to the unit superintendent (US), and that the US I | |||
personally prepared the performance appraisals of the SSs. ! | |||
(Discussed in Section 3 A 1 of this inspection report) { | |||
; | |||
t6 ! | |||
l | |||
4pf ts 3. 0. 3 Actione: The unit superintendent indicated that l ! | |||
there were no operations Department actions which were | |||
anticipated or required within the first three hours of i | |||
i | |||
entering the action statement of TS 3.0.3. The inspection ! | |||
identified that the VEGP management policy and stated practice ! | |||
required preparations for a power reduction, including | |||
i informing the load dispatcher within the first hour. | |||
i | |||
j (Discussed in Section 2.1.1.3 of Inspectica Report 50-424/90- i | |||
; | |||
' its 50-425/90-19) ; | |||
, | |||
a | |||
490 ! | |||
; In summary, the inspection identified these violations and two\ r | |||
' inspector followup items. The violations involved: (1) a violation i | |||
of 10 CFR 50.9 in that responsible licensee officials provided | |||
inaccurate information to the NRC during the inspectionf4(2) a , | |||
violation of TS 6.7.1.a in that, two examples were identified of k | |||
i | |||
i | |||
i | |||
the licensee failing to }mplement actions in accordance with | |||
l administrative procedures /, M _f') : vi:1;ti... . M 0.7 n, . | |||
, | |||
W '. 2, 0: iter!:: "Y!, in th:t, tt:0 ::: ;1 : ::: id:nti f'<ed-of ! | |||
l | |||
th; li;;;;;; i pi::: ting in:d:ptt: ::rr :tiv: ::ti;;;. ' | |||
, ; | |||
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- | |||
LIMITED DISTRIBUTION - Not For Public Release | |||
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- - . - - - - . - - - - _ - . . | |||
. | |||
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. LIMITED DISTRIBUTION - Not For Public R21ccco | |||
DRAFT - PREDECISIONAL INFORMATION | |||
' | |||
The inspection also identified two inspector followup items , | |||
involving: (I) an unreviewed safety question concerning the use of ; | |||
the alternate radwaste building, and (2) the lack of operator | |||
guidance concerning the applicable limiting conditions of operation | |||
during engineered safety features actuation system sequencer ; | |||
outages. | |||
! | |||
! | |||
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4 | |||
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LIMITED DISTRIBUTION - Not For Public Release | |||
* ! | |||
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LIMITED DISTRIBUTION - Net For Public R31easo | |||
DRAFT - PREDECISIONAL INFORMATION | |||
INSPECTION DETAILS l | |||
1.0 INSPECTION OIL 7ECTIVES | |||
Recent activities which have occurred at the Vogtle Electric | |||
Generating Plant (VEGP) have raised concerns within the Nuclear | |||
Regulatory Commission (NRC) as to the ability and the determination | |||
of the licensee to operate the facility in a safe and conservative | |||
manner. To address this concern, the NRC performed a special team | |||
inspection to determine if the licensee operates the facility in | |||
accordance with approvad procedures and within the requirements and | |||
intent of the facility's operating license. In addition to the | |||
occurrence of specific events, NRC concerns regarding the safe | |||
operation of the facility were heightened with the receipt of I | |||
several allegations relating to operational activities at VEGP. l | |||
The aggregation of the facts and circumstances associated with the | |||
operational events and the allegations was viewed as a possible | |||
indicator of a non-conservative attitude on the part of the i | |||
facility's operating staff which warranted the immediate initiation ' | |||
of special inspection activities. | |||
Because a non-conservative attitude or operating philosophy may j | |||
represent a hazard to the health and safety of the public, a l | |||
special inspection team comprising staff from the Region II Office l | |||
and the Office of Nuclear Reactor Regulation (NRR), assisted by ' | |||
staff from the Office of Investigations (OI), was formed to | |||
determine the individual validity and collective impact of these | |||
allegations on the safe operation of the facility. The purpose of l | |||
the inspection was to determine if the licensee operates the j | |||
facility in a conservative and safe manner in accordance with | |||
approved procedures, and the intent and requirements of the | |||
facility's operating license. Specifically, the inspection | |||
objectives were to: | |||
1) kssess the operational philosophy, policy, procedures, and l | |||
! | |||
practices of the facility's operating staff and managemenc l | |||
regarding operational safety. ) | |||
, 2) Determine the technical validity and safety significance of l | |||
each of the allegations and their impact on the safe and ' | |||
, conservative operation of the facility. | |||
l These inspection objectives were accomplished by the use of two | |||
inspection teams--an operations followup team and an allegations | |||
; followup team. The efforts of these two inspection teams were | |||
: | |||
closely coordinated; however, they independently pursued the | |||
obj a::tives outlined above. | |||
LIMITED DISTRIBUTION - Not For Public Release | |||
7 | |||
, | |||
4 | |||
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__ ..___ _.- _ _ _ __ . _ _ _ _ _ . _ _ _ _ _ _ . _ __. - _ _ _ . ~ _ _ _ __ _ | |||
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.. LIMITED DISTRIBUTION - Not For Public Rolosso fr i | |||
l DRAFT - PREDECISIONAL INFORMATION 3- | |||
- | |||
6 | |||
i | |||
j Theoperationsfollowupteammonitoredcontrolroomactivitieson( | |||
: | |||
a 24-hour basis in order to: (1) evaluate the operational 8 ! | |||
- | |||
philosophy, policies, procedures, and practices of the operating 3 | |||
3 ' staff . and management and- (2) determine if the plant was being' . | |||
! | |||
: | |||
operated in a safe and conservative manner in accordance with the g ! | |||
facility's operating license. 3 ! | |||
C , | |||
The specific inspection activities of the operations team was : | |||
described in Inspection Report 50-424/90-19 and 50-425/90-19g e ,. | |||
efforts and conclusions of the allege8 _ti_ ops followup teams are i | |||
described in this inspection report. " In addition, this report } l | |||
identifies several violations 2nd $2;;..;i:1 ;;;%..;;;;; in the l | |||
( | |||
licensee's :;;reti;nci pr!!:ler, prr;r-- , and procedures. 9he- ; | |||
gecificdetails==d h:;i; fe; th; ine;::ti:r trer's r---=ea= are | |||
detailed in the sections that follow and in the Inspection Summary. | |||
, | |||
' | |||
' | |||
2.0 ALLEGATION FOLIDWUP | |||
The inspection team reviewed several allegations for their | |||
[ | |||
technical validity and interviewed licensed and non-licensed ! | |||
personnel to determine their personal knowledge and experience ! | |||
regarding these issues. This portion of the inspection was j | |||
performed to determine the validity and significance of the . | |||
allegations. 5:::r:: the elle;stierr errerted *Mt li--- ed ' | |||
! | |||
:;:::t::: 5:d vieleted the Techair:1 Sp^cificatiene (??) vith the ! | |||
h.:rl:d;: f lieerrer rare;r rrt, *he inepretien t:22 revier:d th: ' | |||
cirrrrrtencer e-d retienele fer i=dividerl retic- . ' | |||
The inspection of the allegations included technical reviews of the | |||
licensee's records, logs, and interviews of the personnel involved | |||
in the alleged violations. Although a transcribed record was not | |||
required for every discussion with the licensee's staff, the | |||
inspection team conducted sworn, transcribed interviews with | |||
selected individuals in order to document (1) the individual's | |||
personal knowledge and involvement in the alleged violations and | |||
(2) the circumstances and rationale for their individual actions. | |||
Although an of investigator was assigned to the inspection team to | |||
assist during the transcribed interviews, this inspection was not | |||
an investigation | |||
ewr cos into .the | |||
ar 7w Anap Aur.sers 5 m intent | |||
Amp.rc ofghe h alleaed vi.olations. TwaM | |||
p c. m n Cnc ,ys s,. | |||
The interviews were transcribed after the technical evaluations of | |||
the allegations in order to permit a focused interview and to | |||
minimize the length and scope of the transcribed proceedings. | |||
, | |||
The | |||
' | |||
transcribed interviews are listed in Appendir 1 in the order they j 4 p | |||
were conducted. The sworn testimony was th? 5;;;6on wnica the | |||
inspection team reached its conclusion on each of the allegations. | |||
These conclusions are prcsented in the material that follows | |||
i | |||
l | |||
(Sections 2.1 through W ). ' ' | |||
2. . B | |||
LIMITED DISTRIBUTION - Not For Public Release i | |||
8 | |||
. | |||
W | |||
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LIMITED DISTRIBUTION - Nct For Public R310000 ' | |||
DRAFT - PREDECISIONAL INFORMATION | |||
; 2.1 .Imoroner Installation of FAVA System | |||
i | |||
: | |||
An allegation indicated that VEGP installed and operated a radwaste | |||
nicrofiltration system, known as the FAVA system, | |||
j without ! | |||
performing an adequate engineering and safety evaluation (i.e.,10 | |||
! | |||
I | |||
CFR 50.59). Furthermore, the material configuration, fabrication i | |||
and quality of the system did not meet the guidance of Regulatory | |||
. | |||
l' | |||
Guide (RG) 1.143 and the requirements of the American Society of | |||
. | |||
Mechanical Engineer's (ASME) Code. | |||
1 | |||
i | |||
The FAVA system was temporarily installed for removing Niobium-95. | |||
i | |||
The system was later determined to be better suited for as-low-as- , | |||
' | |||
i reasonably-achievable considerations during refueling outage IR2, i | |||
particularly for removing Cobalt-59 and Cobalt-60. VEGP planned to | |||
i replace this temporary modification with a permanent, high- | |||
j; quality, steel system in the future; however, the health and safety l | |||
; | |||
of the public may be jeopardized if a break in the system i | |||
; (resulting in a radioactive release to an unrestricted area) | |||
occurred in the interim. i | |||
' | |||
, : | |||
, | |||
j Discussion i | |||
, . | |||
? | |||
! | |||
e | |||
, | |||
- In February 1988, the VEGP experienced difficulty in removing [ | |||
colloidal Niobium-95 following a reactor shutdown for maintenance | |||
work. i | |||
; | |||
; FAVA Control Systems (FAVA) was hired to help rectify this | |||
problem. FAVA was selected because of its experience in filtration | |||
j' | |||
- | |||
and domineralization. The situation was corrected by installing ! | |||
i a 0.35-micron filter system downstream of the existing vendor- | |||
supplied pre-filters. t | |||
i generated as the 0.35-micron filters | |||
However, a large volume of radwaste was I | |||
i rapidly exhibited high | |||
: differential pressure and were required to be changed frequently. | |||
! | |||
The need to change filters frequently also resulted in additional | |||
! | |||
radiation exposure to Radwaste Department personnel. | |||
j Upon evaluation of the performance of the 0.35 micron filter | |||
system, the Radwaste Department felt that the best approach to the | |||
problem was a back-flush, pre-coat filter system. However, no | |||
: | |||
j | |||
operational data was available for a system of this type in this | |||
specific application. FAVA supplied a proprietan Ultra Filtration | |||
3 | |||
; | |||
System (Model No. SFD/E) for testing purposes in order to evaluate | |||
: whether | |||
problem. or not this was a viable and economic solution to the | |||
i The FAVA system was installed before the Unit I refueling | |||
j | |||
outage and was operated under Test Procedure T-OPER-8801. The test | |||
, | |||
system kept liquid effluent releases well below TS limits. on the | |||
basis of an evaluation of test results by the Radwaste, Chemistry, | |||
; | |||
and Engineering Departments, a general work order was initiated to | |||
l purchase a permanent system. | |||
; | |||
. | |||
i | |||
LIMITED DISTRIBUTION - Not For Public Release | |||
] ' | |||
, | |||
e | |||
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LIMITED DISTRIBUTION - Not For Public RalsoD2 | |||
DRAFT - PREDECISIONAL INFORMATION | |||
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1 | |||
In the early part of 1989, a Quality Assurance (QA) Department : | |||
audit identified a significant audit finding involving a | |||
programmatic breakdown in the procurement of the FAVA system and ! | |||
i the failure to meet commitments of the Final Safety Analysis Report | |||
! | |||
(FSAR).- Because of that finding, the FAVA system was removed from | |||
service. In late 1989, the licensee sought to reinstall the FAVA , | |||
i system under a temporary modification because colloidal Cobalt-59 | |||
i and Cobalt-60 had to be removed. The Plant Review Board (PRB) | |||
, | |||
reviewed this temporary modification and several members expressed | |||
] strong objections to it based on the previous QA audit finding. | |||
- | |||
> | |||
; | |||
i Subsequently, a request for engineering assistance (REA) was : | |||
i submitted and a 10 CFR ' 50.59 safety evaluation was performed in | |||
i late 1980. This safety evaluation did not properly address the | |||
i | |||
- | |||
guidance of Regulatory Guide (RG) 1.143 regarding the use of | |||
polyvinyl chloride (PVC) piping.' Therefore, another safety | |||
; evaluation was p rformed in February 1990 to address this issue--- l | |||
j particularly with respect to radiation degradation. | |||
' | |||
2 | |||
The February 1990 safety evaluation specifically stated that the 1 | |||
l | |||
FAVA system did not conform to the criteria of RG 1.143. This | |||
! ' | |||
deviation was found to be acceptable for the following reasons: | |||
; | |||
' | |||
1) The design of the FAVA system had been previously evaluated | |||
! and found to be adequate in the response to REA VG-9057 dated | |||
l November 28, 1989 (log SG-8592). | |||
l 2) The location of the FAVA microfiltration system inside a | |||
i | |||
shielded, watertight vault provided adequate assurance that | |||
; any system failures will be contained and would not create the | |||
l potential for offsite releases of, radioactivity. | |||
. | |||
l 3) The presence of PVC pipe in the FAVA system, although | |||
l- prohibited by RG 1.143, was acceptable because the radiation | |||
i | |||
exposure to the plastic was within acceptable limits for up to | |||
i 6 months based on the following: | |||
; | |||
! | |||
a) The amount of PVC piping used was not extensive and was | |||
j contained on the FAVA filter skid. | |||
1 | |||
i | |||
; | |||
b) There were no reported leaks or malfunctions during the | |||
' approximately 6 months that the FAVA system filter was | |||
previously in use, | |||
d | |||
; | |||
c) Since the FAVA system filter skid was located within the | |||
* | |||
demineralizar vault, it would be protected from being | |||
damaged. | |||
l | |||
) LIMITED DISTRIBUTION - Not For public Release | |||
i | |||
10- | |||
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' LIMITED DISTRIBUTION - Net For Public Raleaso | |||
[, DRAFT - PREDECISIONAL INFORMATION { | |||
l | |||
I d) On the basis of the assumed' length of time that the PVC . | |||
! piping would be used in a radioactive environment and the | |||
: activity levels of the effluent at this stage in the | |||
! liquid radwaste process, the integrated dose to the PVC 'I | |||
: piping would be well below the radiation damage threshold ! | |||
! for PVC pipe as reported in Electric Power Research ' | |||
i | |||
Institute (EPRI) Report NP-2129, dated November 1981 | |||
! (i.e., 6.5 rad over a 6 month period versus the radiation | |||
j: damage threshold of 5.0 x los rad) . | |||
i e) The PVC pipe would not be subjected to excessive pressure ! | |||
i | |||
I | |||
conditions since the maximue. available inlet pressure to i | |||
! | |||
the filter was so to 100 pounds per square inch gauge ! | |||
(psig) which is well below the maximum allowable working | |||
, pressure of 120 psig for the PVC pipe. j | |||
f) The system could be operated at design-basis conditions ! | |||
for 182 days before it would exceed the radiation damage | |||
i | |||
threshold. However, under conditions currently existing | |||
. | |||
at the plant, the expected dose to the PVC piping will | |||
j less than 0.1 percent of the design basis. | |||
i Although the testamony of one of the PRB members indicated that the | |||
, | |||
temperature effects on the use of PVC in the FAVA System were not | |||
i | |||
adequately evaluated before the system was installed, the testimony | |||
! of the corporate system engineer indicated that this was considered | |||
i | |||
prior to installation, although not specifically documented in the | |||
; safety evaluation. | |||
1 | |||
1 | |||
The VEGP general manager subsequently consulted the NRC resident | |||
! inspector to seek an NRC position with regard to placing this | |||
1- system - back in service. This was supplemented by information | |||
{ | |||
' documenting reasons why it should not be placed in service. This | |||
package was forwarded to Region II and the office of Nuclear | |||
Reactor Regulation (NRR) for review. In March 1990, following | |||
Region II and NRR concurrence via a telephone conference, the | |||
licensee placed the FAVA system in service with the following NRC | |||
! stipulations: | |||
I | |||
j 1) Procedures for operating the FAVA system required an operator | |||
, | |||
j | |||
to be in attendance for the entire length of time the systra - | |||
' | |||
would be in operation. | |||
i | |||
. | |||
2) All hoses going to and coming from the FAVA syst en required | |||
! verification that they met the requirements of RG 1.143. | |||
1 | |||
; 3) The cover over the FAVA system wa- required to be securely | |||
; fastened when the system was in operation to ensure that if a | |||
' LIMITED DISTRIBUTION - Not For Public Release | |||
, | |||
11 | |||
1 | |||
) | |||
L | |||
, | |||
D | |||
h | |||
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' | |||
. | |||
- , _ | |||
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__ _ __ __ . _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _._ -_ __ _______ _ ____ | |||
. 4 | |||
' - LIMITED DISTRIBUTION - Not Fcr Public R21eace | |||
DRAFT - PREDECISIONAL INFORMATION - | |||
! | |||
i spraying leak developed, it would be contained in the concrete | |||
l vault. | |||
i- | |||
4) The design of the . walls of the alternate radwaste building ! | |||
! | |||
(ARB) was required to be evaluated to determine whether or not | |||
i a design modification should be made to reduce the potential ? | |||
j of wall leakage in the event that a hose leak developed and | |||
j sprayed its contents on the walls. | |||
, | |||
i In June 1990, in response to item 4 (above), the licensee revised | |||
Part G of the safety evaluation for the FAVA system. Part G of the | |||
i safety evaluation addressed the effect that operation of the FAVA 1 | |||
! system would have on the probability of occurrence or consequences , | |||
{ of accidents described in the FSAR. Although there was no l | |||
4 | |||
comparable accident analysis in the FSAR that addressed the ARB | |||
accidents or the consequences of accidents in the ARB, the FSAR | |||
I accident analyses (Chapters 15.7.2 and 15.7.3) did describe worst- | |||
; case releases of the contents of the recycle holdup tank (HUT) . | |||
l' | |||
The first bounding analysis in Chapter 15.7.2 addressed the release | |||
of the entire gaseous radioactive contents of the HUT to the | |||
i' | |||
environment at ground level and the second bounding analysis { | |||
addressed the release of the entire liquid contents of the HUT- | |||
i through an assumed crack 2n the ARS floor directly into the ground ! | |||
;. water supply. In both cases, the 10 CFR Part 100 and 10 CFR Part 1 | |||
' | |||
20 limits were not exceeded. These criteria were consistent with | |||
' | |||
j criteria provided in NRC Circular 80-18, "10 CFR 50.59 Safety l | |||
Evaluations for Changes to Radioactive Waste Treatment System." ' | |||
: However, neither of these analyses addressed the potential for wall | |||
: spray down and leakage. through the ARB walls and the subsequent | |||
t release path to the environment. Therefore, the licensee revised | |||
the safety evaluation in June 1990 to address the consequences of | |||
i | |||
a hose break on the FAVA system which would result in wall spray | |||
l | |||
down and potential leakage to the environment. | |||
, | |||
l The inspection team's review of the revised Part G of the safety | |||
i evaluation identified several erroneous assumptions with respect to | |||
the release path and the dilution volumes that could be used in the | |||
, | |||
analysis of a hose break and resultant wall spray down. However, | |||
; | |||
the inspection team also found that the design of the FAVA system | |||
; (i.e., the use of a system cover) would prevent wall spray down and | |||
; | |||
that the only potential source for wall spray down and subsequent | |||
leakage was from a hose break in another radwaste system in the | |||
: ARB. Therefore, the inspection team concluded that the FAVA system | |||
safety evaluation dated June 1990, adequately addressed the | |||
. | |||
temporary modification for the installation of the FAVA system; | |||
j however, the inspection team's review identified an unreviewed | |||
4 | |||
; LIMITED DISTRIBUTION - Not For Ptblic Release | |||
, | |||
12 | |||
i | |||
! | |||
! | |||
! | |||
. | |||
. | |||
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. | |||
, | |||
- | |||
l | |||
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l | |||
. | |||
LIMITED DISTRIBUTION - Not For Public RoloaSG l | |||
DRAFT - PRIDECISIONAL INFORMATION | |||
safety question concerning the release paths and consequences of a ! | |||
failure of the other radwaste systems in the ARB. | |||
In' addition, the team noted that in Supplements 3 and 4 of the | |||
Safety Evaluation Report (SER), the NRC staff reviewed and accepted , | |||
, | |||
the design of the ARB and specifically addressed the consequences | |||
of a hose break on a radwaste system in the ARB. However, the SER | |||
supplements addressed the effects of high airborne activities and | |||
, | |||
puddling and did not address the potential for wall spray down and | |||
leakage. The ARB was installed before the plant was licensed; | |||
t | |||
' therefore, the NRC approved the design and use of the ARB in ) | |||
Supplements 3 and 4 of the SER. Thus, there was no requirement to ! | |||
perform another evaluation of the potential effects of hose brcaks | |||
on systems other than the system being installed by the temporary | |||
modification (i.e., the FAVA system). | |||
1 | |||
Because the design of the | |||
l | |||
FAVA system effectively prevented a wall spray down, this was not ; | |||
' a concern that was required to be addressed by the FAVA system ' | |||
safety evaluation. Nevertheless, now that it has been identified, | |||
l | |||
l the consequences of a hose break and wall spray down in the other | |||
4 | |||
ARB radwaste systems must be resolved. Therefore, this issue will | |||
be followed as an inspector followup item pending further review | |||
and evaluation and is identified as: | |||
;' 19 -14 19 - N | |||
IFI 50-424/90.x*-07 and 50-4 2 5/ 9 0-xw-02", 'Dotential Unreviewed | |||
Safety Question Regarding Spray Down of the Alternate Radwaste | |||
Building." . | |||
J | |||
< | |||
; Conclusion l | |||
Although the FAVA system was originally installed without an | |||
3 | |||
adequate safety evaluation and did not meet the regulatory l | |||
guidance, the inspection team concluded that the subsequent safety i | |||
evaluations were acceptable for the system's use. Serefert, th; | |||
1 | |||
' inerrtien tem cen:1 d:d that th; ellgeti;n iter ne* M 1y ) l | |||
r Arte el.i d. ( | |||
: | |||
As a result of QA Department's significant audit finding in early | |||
1989 involving a breakdown in procurement and failure to meet FSAR | |||
: commitments, the system was removed from service. Subsequently, ; | |||
the FAVA system was returned to service following two safety j | |||
, | |||
evaluations which adequately addressed the use of PVC piping with I | |||
respect to radiation degradation and pipe rupture. Therefore, | |||
these safety evaluations justified the use of the FAVA system, even | |||
though the recommendations of RG 1.143 and ASME Code requirements | |||
were not met. Although the safety evaluations did not specifically | |||
address high-temperature effects, the testimony indicated that | |||
these effects had been considered before the system was installed. | |||
i | |||
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DRATT - PREDECISIONAL INFORMATION | |||
Although the safety evaluation performed in June 1990 at the | |||
, request of the NRC Region II Office did not adequately evaluate the | |||
! | |||
effects of a wall spray down and wall leakage to an unrestricted | |||
area, this evaluation was not required because the FAVA system has | |||
a protective cover and the use of hoses and effects of hose breaks | |||
(i.e., airborne activity and puddling) were addressed in SER | |||
J | |||
Supplements 3 and 4. | |||
I | |||
Regardless of whether the safety evaluation was required to address | |||
the effects of a break in the hoses (which could result in wall | |||
spray down or leakage), the inspection team identified a new | |||
concern involving the use of the ARB because the safety evaluation | |||
inadequately addressed the potential effects of wall spray down | |||
l from any other source in the ARB owing to erroneous assumptions | |||
; concerning the release path and the dilution volumes. This is a | |||
< | |||
potentially unreviewed safety question concerning the use of the | |||
alternate radwaste building. | |||
2.2 Operability of the Residual Heat Removal Pumo | |||
; | |||
' | |||
An allegation indicated that during Unit i refueling outage IR2 | |||
with residual heat removal (RHR) Train A out of service for | |||
maintenance, the Train B RHR pump experienced excessive vibration | |||
and a nuclear service cooling water (NSCW) motor cooler outlet | |||
i | |||
i | |||
leak. In addition, TS 3.9.8.1, "RHR and coolant Circulation," was | |||
allegedly violated because the operations Department chose not to | |||
, declare RHR pump 15 inoperable in an effort to mitigate the impact | |||
on the critical work path. | |||
Discussion | |||
TS 3.9.8.1 requires at least one RHR train to be operable and in | |||
operation during Mode 6 (refueling) when the water level above the , | |||
top of the reactor vessel flange is 23 feet or more. Otherwise, ' | |||
Suspeed all operations involving an increase in the l | |||
reactor decay heat load or a reduction in boron i | |||
, | |||
concentration of the reactor coolant system (RCS) and j | |||
! | |||
Immediately initiate corrective action to return the ' | |||
I | |||
required RHR train to operable and operating status as | |||
soon as possible and close all containment penetrations | |||
' | |||
providing direct access from the containment atmosphere | |||
to the outside atmosphere within 4 hours. | |||
The inspection team verified that during Unit I refueling outage | |||
IR2 with higher than normal vibration measurements on the RHR pump < | |||
4 | |||
1B and a leak on the NSCC outlet of the Rh motor cooler, | |||
Department did | |||
' | |||
operations personnel not declare the pump ; | |||
LIMITED DISTRIBUTION - Not For Public Release I | |||
14 | |||
I | |||
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e | |||
'__.__._.______.___..________.--- | |||
__ _ . _ . ___ _ _ .. . _ _ . . - . _ _ _ ________ | |||
f | |||
. | |||
* | |||
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,, | |||
LIMITED DISTRIBUTION - Nat For Public R21ecco | |||
, DRAFT - PREDECISIONAL INFORMATION | |||
i | |||
i inoperable. This determination was made after consulting with the | |||
# | |||
on-shift duty engineer from the Engineering Department and was ! | |||
, based on the determination that the pump would fulfill its intended ' | |||
j | |||
!, | |||
safety function in Mode 6. Specifically, the RHR pump was capable | |||
of removing decay heat from the partially defueled reactor core. | |||
j The testimony of the individuals involved indicated that this . | |||
. operability determination was based on the fact that the vibration | |||
; readings taken at the inservice test (IST) surveillance points did | |||
not reach the IST Alert levels and were therefore acceptable for | |||
: continued service. Although the high vibration readings on the top | |||
. | |||
end of the RHR pump were later determined by the vendor | |||
- | |||
(Westinghouse) to be excessive, at the time of the operability i | |||
: evaluation, the licensee accepted these values, regardless of their | |||
f | |||
magnitude, because the readings at IST test points were below the | |||
I Alert levels. The testimony also indicated that, even with a leak l | |||
l on the NSCW outlet of the RHR motor cooler, the motor was receiving ' | |||
j full cooling water flow and cooling would not have been immediately | |||
i compromised following a complete NSCW discharge pipe break. | |||
l Furthermore, the. testimony indicated that the operations Department | |||
j had : implemented compensatory actions to monitor the vibration | |||
: levels and NSCW 1eakage and ensure the continued operability of the | |||
l pump by stationing an operator at the RHR pump to monitor the | |||
: vibration levels and notify the control room if the vibration | |||
, | |||
levels increased, thus allowing the control room to implement the | |||
actions of the limiting condition for operations (140). | |||
: | |||
The inspection team also noted that in event of a catastrophic | |||
! | |||
failure of the RHR pump, all the required actions of TS 3.9.3.I i | |||
I | |||
(i.e., closing all containment penetrations) | |||
' | |||
could have been | |||
$ | |||
completed within the required 4 hour time period of the 140 because | |||
- | |||
' | |||
the Ito for TS 3.9.4, " Containment Building penetrations," was in | |||
effect during this time period. This LCO was implemented due to | |||
, | |||
the movement of irradiated fuel from the core to the spent fuel | |||
j | |||
4 | |||
pool. The 140 required that, | |||
The equipment door be closed and held in place by at | |||
least four bolts; at least one door in each airlock be | |||
; | |||
closed; and each penetration providing direct access from | |||
1, | |||
the containment atmosphere to the outside atmosphere | |||
i shall be either closed by an isolation valve, blind | |||
; | |||
. | |||
flange, or manual valve, or be capable of being closed by ' | |||
an operable automatic containment ventilation isolation | |||
j valve. | |||
4 | |||
: | |||
As a result of the implementation of TS 3.9.4, the only remaining | |||
act' .n for the LCO of 73 3.9.8.1 would have been to close the | |||
} | |||
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. | |||
: 15 | |||
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4 | |||
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. .- .. - - . . - - _ . . - _- -- .. -. - - .-. - . . - _ . - - - . . - - | |||
i , | |||
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j | |||
j. LINITED DISTRIBUTION - Not For Public R21 ease j | |||
; DRAFT - PREDECISIONAL INFORMATION ' | |||
containment purge valve which receives an automatic closure signal * | |||
' | |||
and could have been isolated within the Iro action times. ! | |||
4 During the course of this review, the inspection team found that | |||
the licensee failed to initiate a deficiency card for either the ! | |||
i NSCW 1eak or the excessive vibration as required by operations ! | |||
4 Procedure 00150-C, " Deficiency Control." This procedure requires i | |||
' | |||
i that a deficiency card be written if the deficiency involves | |||
; safety-related components which are to be dispositioned "use-as- i | |||
i is/ repair," or other conditions involving safety-related components , | |||
which require engineering suppolt or other technical assistance to i | |||
determine if the component is deficient. Failure to establish, | |||
, | |||
implement, and maintain adequate operating procedures represents a , | |||
1 violation of TS 6.7.1.a. This item is identified as: | |||
R-G 6 I | |||
; | |||
.' VIO 50-424/90_xx=Gt,i..a ;; = /;0 m ;i, " Failure To Establish or | |||
l Implement Procedures for Required Activities." | |||
h conclusion , | |||
! | |||
! | |||
The inspection team c luded tht t.5e 11-v. tis, n; n;t frily ' | |||
i c ertentistrf L;;.;;.3 e operations Department had an adequate i | |||
! engineering basis for accepting the operability of the RHR pump in | |||
j spite of the pump's deficiencies. In addition, the team concluded i | |||
j that declaring the pump inoperable would not have impacted the | |||
! critical work path: the 140 actions would not have been restrictive | |||
' | |||
because containment (excluding ventilation) had been isolated as | |||
, | |||
, required by TS 3.9.4. The LCO actions would not have prev . ,ad the | |||
: continuation of refueling activities because the actions to close ! | |||
: all containment penetrations providing direct access from the ! | |||
containment atmosphere to the outside atmosphere would only have 1 | |||
required closing the containment purge valve which has an automatic | |||
closure signal. | |||
l In addition, the inspection team identified that the licensee | |||
; violated the station's administrative procedures by failing to | |||
, | |||
initiate a deficiency card for either the NSCW outlet leak or the | |||
; excessive vibration on the RNR motor as required by Operations | |||
' | |||
t | |||
Procedure 00150-C. | |||
, | |||
-?' "!:rrf cert fr ent I:02: tier V:1:: Ourec ill;; ca - | |||
l An allegatio icated that a unit shift isor (USS) | |||
concealed the correc time for a T o prevent a forced | |||
i- shutdown of the unit and to ' | |||
CFR 50.72 notification to | |||
: the NRC. Furthermore, c ent . ion valves (CIVs) which | |||
' | |||
were missed durin rveillance test sho va been declared | |||
!- inoperabl e immediata actions of the TS LCO s ave been | |||
1 i at the time the missed surveillance was identifie . | |||
1 | |||
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16 l | |||
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L i | |||
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- - . - . - . --- --. -..-._ - . . - - -._- -- .--- | |||
4 | |||
* | |||
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l | |||
. | |||
DRAFT - PREDECISIONAL INFORMATION | |||
ddition, delaying the initiation of the deficiency card (DC) unt 1 : | |||
i. | |||
* | |||
t surveillance had been re-perfonned allowed the licensee o i | |||
av (d the immediate actions of the LCO and allowed the un to i | |||
) rema'in in operation and avoid the immediate NRC notificatio . | |||
Discus on | |||
! The inspe tion team reviewed the documentation of a missed | |||
j | |||
surveillanc on the containment isolation valves escribed in | |||
a Licensee Eve Report (LER) 90-001 for which a non- ted violation ; | |||
(50-425/90-01- 1) was issued. The LER identified hat during the | |||
i review of mont y Surveillance Procedure 1447 -2, " Containment > | |||
! | |||
' | |||
Integrity Veriff tion-Valves outside Contain nt," the licensee : | |||
discovered that 3 CIVs had been overlook and had not been | |||
i tested. In additi , | |||
the valves had not b en tested during the | |||
< | |||
previous two month 1 s surveillances. Up identification, the | |||
j operating shift re-performed the com ete surveillance and | |||
; | |||
initiated an investigat n which resulte in a deficiency card (DC) | |||
! | |||
for the previously misse surveillance . | |||
i | |||
i | |||
root cause of the violation was | |||
, | |||
8 | |||
The LER indicated that t | |||
personnel error in reviewing t e co lated surveillance task sheet. i | |||
In addition, the computer softv which generated the surveillance | |||
l- task sheets (STS) has been a ified so that it is no longer | |||
! | |||
' | |||
possible to inadvertently t n incomplete listing of the | |||
equipment. Even if an error imil to the one which resulted in | |||
. | |||
# | |||
only two valves being shown n the S were to recur, it could only | |||
result in either all or n e of the e ipment being listed, | |||
i The inspection team v rified that S 3.6.1.1, " Containment | |||
! Integrity," 140 actio statement requi d restoring containment | |||
l integrity within 1 ur or commencing unit shutdown to hot | |||
- | |||
standby within the n t 6 hours. A shutdo required by Technical . | |||
Specifications wou d have required that th NRC be immediately | |||
s | |||
notified in accor ance with 10 CFR 50.72. | |||
! | |||
' | |||
The inspection aan found that the CIV surveillance requirement of | |||
i TS 4. 6.1.1. a ad been completed and approved. The surveillance | |||
, procedure r ired verification every 31 days that al penetrations | |||
i | |||
not capabl4 of being closed by operable containee t automatic | |||
i isolation / valves and required to be closed durin accident | |||
conditi ns be closed by valves, blind flanges, or d etivated | |||
) | |||
' | |||
autom ic valves secured in their normal positions. Du ing the | |||
next shift, the oncoming shift supervisor noted th the | |||
su elllance procedure was only partially performed and that 9 of | |||
' | |||
t CIVs on the surveillance procedure had been marked as ot | |||
pplicable" and had not been performed. | |||
; | |||
' | |||
a | |||
. . | |||
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4 | |||
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17 | |||
5 | |||
_ | |||
. | |||
t | |||
O | |||
- | |||
- --, - . .. | |||
. - + - - - ~ - " ' ' | |||
- | |||
l. | |||
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DRAFT - PREDECISIONAL INFORMATION | |||
!' | |||
TS\.0.2.a | |||
witft4n therequires | |||
specifiedthattimeeach | |||
intervalsurveillance requirement be perforud | |||
exten) with a maximum allowa ee | |||
ion not to exceed 25 percent of the surveillance inte | |||
In aditition, Ts 4.0.3 requires that al. | |||
failure to perf | |||
survell | |||
constitut | |||
nee requirement within the specified time interva shalla | |||
LCo. As a failure to meet the operability requirement for an | |||
uch the failure to perform Surveillance R irement | |||
4.6.1.3.a fk a,ll the CIVs within the surveillance pari (i.e. | |||
days plus the 25-percent extension) would have co tituted ,an 31 | |||
inoperable con' ition of the CIVs. | |||
The oncoming USS | |||
determine if the stified that he lacked sufficie information to | |||
omplete surveillance had n been performed | |||
within the survalliance frequency because he w | |||
the | |||
circumstances under which the surveillancenot | |||
performed. | |||
familiar with | |||
procedure was | |||
Furthermorg, he lacked sufficient information in the | |||
control | |||
had beenroom to deterni | |||
performed withine if the complete. surveillance procedure | |||
his experience, the CIV su he surveillance ' period. On the basis of | |||
eillance was mormally performed in its | |||
entirety; therefore, the potential existed that another partial | |||
surveillance | |||
CIVs. Although procedure had verified the position of the missed | |||
the control room,previously performed surveillances were filed in | |||
neither controlled these records' era | |||
nor complete. ' for information only and were | |||
' | |||
The USS indicated that the previou stwo monthly surveillances on | |||
the CIVs obtained from this ' file sqre performed incompletely; | |||
however, he did not know whether surveillances on the missed CIVs | |||
had been performed completely under \some other surveillance | |||
procedure. | |||
This was confirmed when tNe team interviewed the | |||
surveillance coordinator! Who indicated that approximately once a | |||
missed surveillances were performed under different tasks. mo | |||
Upon identificatiop/ \ | |||
of the potential missed surVtillances the USS | |||
had actually b en missedtoand, | |||
initiated an inveftigation determine whether the surve,illances | |||
concurrently, r -performed the | |||
surveillance | |||
the discove w hin three hours. The inspection tea verified that | |||
time at whi time on the deficiency card correctly flected the | |||
had been p it was verified that the previous two s elllances | |||
formed incompletely. | |||
Cone sion | |||
, | |||
On the basis of the testimony of the USS, the inspection te | |||
neluded that the allegation was not fully substantiated becaus | |||
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18 | |||
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--_. . - . .. | |||
4 | |||
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' | |||
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LIMITED DISTRIBUTION - Nst For Public Release | |||
, DRAFT - PREDECISIONAL INFORMATION | |||
USS did not conceal the true discovery time of the sis CIV | |||
surve ces to avoid a unit shutdown. The USS indi that he | |||
' | |||
was not pre ed to keep the plant in operation o prevent NRC | |||
notification. stated that he had er been given any | |||
indication or instruc to do " wha r it takes" to kecp the | |||
; | |||
unit on line or to avoid N t ation of unusual events. The | |||
USS did not know and co no onfirm if the previous CIV | |||
surveillances had been equately per ed and believed that the | |||
surveillance co re-performed within allowable outage | |||
time; ther , his actions to initiate an invest on into the | |||
4 | |||
" | |||
adequ of the previous surveillance and to concur re- | |||
ora the CIV surveillance procedure were appropriate. | |||
: : ":f: chance 9fth Inemable source -Jtanae- Monitor Mucien | |||
f Instrument | |||
1 | |||
1 An al gation indicated that the operations staff allege | |||
' | |||
knowing violated Technical Specifications (TS) when the uni as | |||
taken fro Mode 5 (cold shutdown) to Mode 6 (refueling) th a | |||
i | |||
source rang monitor (SRM) nuclear instrument inoperable d that | |||
the prohibite operational mode change was made in orde o reduce | |||
the critical pat outage time. | |||
! Discussion | |||
i | |||
' | |||
The inspection team rev ved the documentati of the mode change | |||
' described in Licensee Eva Report (LER) 90 04 for which non-cited | |||
Violation 50-424/90-10-03 s issued. e LER indicated that TS | |||
3.0.4 was violated on March 1990, en Unit 1 entered Mode 6 | |||
* | |||
from Mode 5 with an 140 for Sou e Ra .ge Channel IN31 in effect to | |||
allow performance of an 18-mont 'hannel calibration. The LER | |||
indicated that the root cause to t avant was personnel error by I | |||
the shift superintendent. | |||
The inspection team confir'med that TS 310.4 required that entry | |||
i into an operational mode not be made unlesssthe conditions for the ; | |||
' | |||
. LCO are met without aeliance on the provisions of the action | |||
requirements. With.one source range monitor inoperable, TS 3.9.2, | |||
" Instrumentation,' could not be satisfied in\ Mode 6 without | |||
reliance on the' action statement. | |||
' | |||
/ | |||
Personnel w[re interviewed to (1) confirm the effect on the outage | |||
scheduled /irectly attributed to this TS violation, (2) etermine | |||
whether'it was known at the time of the mode change that mode- | |||
i restraining LCO was in effect, and (3) determine the exte t of | |||
, | |||
phasis on schedule. | |||
: | |||
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19 | |||
. | |||
G | |||
_. - _ _ _ _ _ _ . _ _ . . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ , | |||
_ _ . - _ . _ . ._ _ . _ _ _ . . _ ._._._._ _ ._ _ _._ _ _ _ _ _ _ _. _ _ | |||
! ! | |||
i. . | |||
! | |||
LIMITED DISTRIBUTION - Nst Fcr public Ralocco | |||
; . DRAFT - PREDECISIONAL INFORMATION / ! | |||
. | |||
I | |||
The testimony and a review of the outage schedule confirmed tha ( | |||
; | |||
ere was a reduction in critical path outage time which w ! | |||
: d the l | |||
! SRM ectly o anattributed | |||
operable status. to proceeding to Mode 6 before restoring / | |||
i l | |||
. i | |||
l The te isony also indicated that the shift superintendent (SS) and | |||
{ .the uni shift supervisor (USS) did not recognize that 'a mode- | |||
j restrain LCO was in effect at the time of the mode change. Both | |||
! | |||
the SS and SS were aware that there was an active 140 on the SRM, | |||
, | |||
but neither f them had connected the LCO to the mode., restriction. | |||
i | |||
i | |||
contributing ctors to the error were that both th 8 and USS had | |||
directed their attention to a problem with the esting of the : | |||
) engineered safet features actuation system (ES ) sequencer and i | |||
i that the-work whi had been emphasized to be 1 ding up the mode ! | |||
< | |||
change was the d ontamination of the redctor head. Upon i | |||
j notification that th Health Physics Department had cleared the l | |||
; | |||
; | |||
reactor head for work, the SS granted permission to enter Mode 6. i | |||
, | |||
i | |||
i | |||
The testimony also indic | |||
unreasonable emphasis on t | |||
ed that there 'was no indication of an ; | |||
critical path schedule. Both the SS ; | |||
- | |||
and USS indicated that they had never been given any indication or ' | |||
! | |||
' | |||
instruction to do "whatever i takes" to stay on schedule. They | |||
I | |||
also indicated that they did t , feel undue pressure to stay on | |||
schedule and, particularly, not , f it meant compromising safety. | |||
, | |||
, | |||
! / ! | |||
The SS admitted that he was initia ly commended for the schedule ' | |||
j benefits; however, the violation of he Technical Specifications | |||
' | |||
was not recognized at the time. Thg SS indicated that he had . | |||
: initially received some sitive fee ack during the morning | |||
! management briefing for a shift's acco lishments and later in | |||
! the briefing the TS vio ation was recognize and discussed. In the | |||
l SS's opinion the re nition of the TS olation negated all , | |||
; positive feedback. | |||
a | |||
] The inspection t an identified an additional c cern during the | |||
inspection conc ning the format and use of the | |||
' | |||
status sheets. | |||
On the basis interviews with the SS and USS a the review of | |||
; the format o the 140 status sheets, the inspection as concluded | |||
i that both a format and normal use of this form co ributed to | |||
this TS v lation. | |||
i | |||
j | |||
The LC status sheet, is a two-sided form; the section for quired | |||
actio a begins on the front and continues on the back, who the | |||
; "re rks" section is located. During the testimony, both t | |||
i an USS indicated that their usual practice, notwithstanding a SS | |||
; | |||
e | |||
anges, was to review only | |||
restorative actions were noted on the back. In this case, the mode | |||
the front of this form because onk | |||
; | |||
1 | |||
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20 | |||
4 | |||
4 | |||
:. - | |||
: | |||
- | |||
l | |||
4 | |||
, . , . . , - - . - , _ - - | |||
8 | |||
. | |||
'' LIMITED DISTRIBUTION - Not For Public ReleaS3 | |||
DRAF"r - PREDECISIONAL INFORMATION | |||
! | |||
seestraint | |||
ion. was noted on the back of the form in the " remarks" , | |||
l | |||
LER 90 4 did not identify the format and use of the LCO st us | |||
sheet, as cause of the violation therefore, corrective ions | |||
, | |||
have not ye een i:aken in this regard. The failure to dentify , | |||
and implement dequate corrective actions to preclude repetition is | |||
a violation of l'O.CFR 50, Appendix B, | |||
Actions," and as s(uch will be followed as: Criterion XVI/ " Corrective | |||
: | |||
VIO 50-424/90-xx-03, "F | |||
, | |||
s | |||
ure To Determine and' implement Adequate ! | |||
Corrective Actions." ' | |||
! | |||
Conclusion N j | |||
! | |||
' | |||
, | |||
onthebasisofthetranscribed,Jnkerviewsandfromitsreviewof | |||
the outage schedule, ) | |||
the i pectionsteam concluded that the | |||
allegation was not fully s stantiated. N.The testimony indicated ; | |||
' | |||
that the mode change w a critical pathsites. However, the | |||
testimony of the shift | |||
perintendent and the unit shift supervisor | |||
involved indicated that at the time of the mode' change they were | |||
not aware that an'Ir0 was in effect on the SRM a that a mode | |||
change was pro ited. | |||
The ins | |||
the ion team also concluded that the corrective act | |||
failed to identify that the format and use of thns for | |||
140 | |||
sta sheets, was one of the causes of the event. Therefore, e | |||
f | |||
ure to implement appropriate corrective actions was found to | |||
, | |||
violation of 10 CFR 50, Appendix. 8, Criterion XVI. | |||
2.b pr Backdatino of sianatures | |||
An allegation indicated that a temporary change to Abnormal | |||
Operating Procedure (AOP) 18028-C, "Ioss of Instrument Air," was | |||
not approved within the 14-day requirement of TS 6.7.3.c; and that | |||
the unit superintendent intentionally incorrectly signed and dated | |||
the | |||
' | |||
, | |||
temporary change to indicate that the TS requirement was | |||
satisfied. | |||
j- Discussion | |||
TS 6.7.3.c requires that temporary changes to AOPs which do not | |||
4 | |||
involve changes to the intent of the original procedure be | |||
documented | |||
within 14 days and | |||
of reviewed in accordance with TS 6.7.2 and approved | |||
implementation. TS 6.7.2 requires that changes | |||
to AOPs be reviewed as stated in administrative procedures and | |||
approved | |||
Administrative by theProcedure | |||
Plant Review Board (PRB) and gener11 manager. | |||
00100-C, "Cuality Assurance Records | |||
j LIMITED DISTRIBUTION - Not For Public Release | |||
21 | |||
4 | |||
1 | |||
. | |||
i- i | |||
I | |||
_ _ _ _ . _ _ _ _ _ _ _ _ _ _ _ . . _ . _ . . _ . _ _ _ . _ _ . _ _ _ _ . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ . _ _ . | |||
w e | |||
', | |||
LIMITED DISTRIBUTION - Not For Public R31saco i | |||
DRAFT - PREDECISIONAL INFORMATION | |||
j Administration," Paragraphs 4.1.1.4 and 4 .1.1. 8, require ~ that | |||
' | |||
i corrections to Quality Assurance records exhibit necessary and | |||
; appropriate signatures, initials, and dates. | |||
! | |||
i operations Procedure 18028-C, Revision 7, provided operator actions : | |||
. | |||
in the event of a loss of the instrument air system. A temporary ' | |||
j change to the procedure was initiated on May 29, 1990, to delete | |||
i the references to the header isolation at 70 psig and the | |||
i associated actions. This change was processed in accordance with | |||
: Administrative Procedure 00052-C, " Temporary Changes to : | |||
i | |||
Procedures," which allowed the temporary implementation of minor i | |||
j | |||
' | |||
changes to procedures as long as the change was approved by the PRB j | |||
and signed by,the general manager within 14 days of the temporary | |||
change. Therefore, Temporary Change Procedure (TCP) 1802-C-7-90-1 | |||
was required to be approved by the PRB and signed by the general | |||
, | |||
) | |||
manager by June 12, 1990. ' | |||
l | |||
'! The PRB tabled the TCP on June 8, 1990, (PRB meeting 90-81) and i | |||
j assigned action to the Operation's Department to void the TCP or | |||
revise the TCP to incorporate the PRB comments. Revision 8 to | |||
] Operations Procedure 18028-C was developed to modify valve numbers | |||
; and descriptions reflected in Temporary Modificatiors 1-90-006 and | |||
i 2-90-002. This revision superseded the changes of the TCP. On | |||
i June 12, 1990, the PRB approved Revision 8 (PRB meeting 90-82) and | |||
! | |||
the TCP was removed from the control room copies of the procedure. | |||
] On June 15, 1990, the unit superintendent lined out the operations | |||
. | |||
manager's previous approval of the TCP and marked the TCP form as | |||
! disapproved by the operations Department. The date entered on the | |||
! form was June 12, 1990. | |||
I | |||
j On June 22, 1990, the PRB secretary initiated Deficiency Card (DC) | |||
; | |||
1-90-282 which indicated that the unit superintendent incorrectly | |||
i | |||
dated the TCP with the date of June 12, 1990, rather than actual | |||
; date of June 15,1990, and DC 1-90-283 which indicated that the TCP | |||
j' was not processed within the required 14 days (i.e., by June 12, | |||
, | |||
1990). The resolution of these DCs, the associated PR8 meeting | |||
i | |||
minutes, and discussions with the operations manager and Nuclear I | |||
Safety and Compliance Department staff indicated that described l | |||
deficiencies were acknowledged and confirmed by the Operations | |||
! Department on July 3,1990, and attributed to personnel error. The | |||
I TCP form was dated with the date on which the Operations Department | |||
l decided to void the TCP and not the date on which the original was | |||
j actually signed. l | |||
As part of the corrective actions for DC 1-90-282, a TCP record | |||
, | |||
correction notice was initiated to correctly indicate the date on ' | |||
! which the TCP fo11 was pro..ssed; however, tus TCP record | |||
l, | |||
correction notice could not be produced--one was subsequently | |||
' | |||
LIMITED DISTRIBUTION - Not For Public Release | |||
; 22 | |||
! | |||
l | |||
e | |||
4 * | |||
; | |||
_ | |||
_ _ . . _ _ _ _ _ _ _ _ . _ _ _ _ . _ . _ _ _ _ _ . _ _ . _ _ _ _ _ . _ ~ _ _ _ . _ _ _ _ _ | |||
j. * | |||
l | |||
:. LIMITED DISTRIBUTION - Nst For Public Ralecao I | |||
: DRAFT - PREDECISIONAL INFORMATION 3 | |||
! | |||
4 written on August 14, 1990. In addition, the operations manager | |||
;- counselled the unit superintendent and assigned him to investigate ! | |||
; both DCs because he was the most knowledgeable of the deficiencies ; | |||
; and the assignment served to reinforce the reprimand. ' | |||
The | |||
4 | |||
subsequent PRB meeting of June 28, 1990, (PRB meeting 90-90) | |||
; determined that the 14-day TS violation addressed in DC 1-90-283 | |||
. was reportable to the VEGP vice president, but not to the NRC. | |||
1 However, the inspection team found that the report to the VEGP vice | |||
i president was not made.- On August 9, 1990, the PR8 (PRB meeting | |||
}. 90-104) confirmed that the report was required. As of August 17, ! | |||
i- 1990, ~ the licensee had not issued the required . cport to the VEGP | |||
j vice president; however, the licensee intended to issue the report. > | |||
, | |||
With respect to the rationale for the unit superintendent's ; | |||
; | |||
actions, the inspection team learned (during discussions with the ' | |||
}. Technical Support Manager) that the PRB secretary told the unit | |||
i superintendent on June 15, 1990, that the TCP needed to be voided | |||
and 4 DC written for violating the 14-day requirement of TS 6.7.3. | |||
l As discussed in Section 2.11 of this inspection report, Operations | |||
i Department personnel are held personally accountable for violations | |||
'- | |||
and LERs (i.e., there is a direct impact on their bonus pay); ; | |||
therefore, a reportable occurrence based on this event could have ! | |||
i | |||
adversely impacted the unit superintendent's salary. | |||
l | |||
l The testimony of the unit superintendent indicated that he dated | |||
: the TCP with the date (June 12, 1990) on which the PR8 disapproved | |||
I it and not the date on which it was actually signed (June ' 15, | |||
i 1990). Additionally, the unit superintendent had no recollection | |||
l of any discussions on June 15, 1990, regarding violation of the 14- | |||
l day TS requirement. He indicated that he never considered the 14- | |||
day requirement despite his previous knowledge and training | |||
i | |||
' | |||
concerning this requirement and the June 12, 1990, expiration date | |||
indicated on the TCP form. | |||
i | |||
! | |||
The testimony of the PRB secretary indicted that during a | |||
! | |||
' discussion with the unit superintendent on June 15, 1990, she ; | |||
identified the need to void the TCP, as well as the need to write ' | |||
!. a DC for violating the 14-day TS requirement. Therefore, the | |||
; inspection team was concerned about whether the TCP was voided | |||
j' before or after the PRB secretary identified the need to void the | |||
! | |||
' | |||
TCP and initiate a DC. In order to resolve this discrepancy, the | |||
inspection team discussed the discrepancy with the PRB secretary on | |||
,. August 16, 1990. In addition to earlier testimony, the PR8 | |||
secretary indicated that during her discussions concerning the TCP | |||
' | |||
' | |||
' | |||
with the unit. superintendent on June 15, 1990, the unit | |||
superintendent had indicated that the TCP had already been voided | |||
j aar13 : in the day. | |||
, | |||
LIMITED DISTRIBUTION - Not Tor Public Release | |||
j 23 | |||
L | |||
! | |||
i- | |||
e | |||
i | |||
! | |||
. . _ _ ._ ~ | |||
. - - - _ - - - . - .. . - -- - . . | |||
- . - - _ . - . - - - . ~ . .. - - . | |||
4 | |||
!, . | |||
;. LIMITED DISTRIBUTICN - Nst For Public Rslossa | |||
DRAFT - PREDECISIONAL INFORMATION | |||
; conclusion | |||
i | |||
l On the basis of the testimony, the inspection team concluded that | |||
; backdating to avoid a violation of the 14-day TS requirement was | |||
I not '0117 ="h-"-ti tted T= idditi^=, the r^ cer- th t ibis | |||
i practice m- a plant-wide problem,==- et *"11 y =nh=* =-t itt ed . | |||
i However, the inspection team did confirm that TCP 1802-C-7-90-1 had | |||
! been dated incorrectly; this was a violation of Administrative | |||
i Procedure 00100-C, " Quality Assurance Records Administration," | |||
! Paragraphs 4.1.1.4 and 4.1.1.8 and will be followed as: | |||
! 19-l's tq -G | |||
' VIO 50-424/90-xx-@2' and 50-425/90-mm-er, " Failure to Establish or | |||
Implement Procedures for Required Activities." \ 1 | |||
l | |||
l | |||
< | |||
g y Reportability of Previous Enaineered Safety Features Actuation | |||
System Load Seauencer outaaes ! | |||
An allegation indicated that the operations Department incorrectly l | |||
used a 72-hour shutdown requirement when one of the two ESFAS load | |||
: sequencers was previously inoperable. It was also indicated that | |||
l VEGP had taken no action to ensure that the past occurrences were , | |||
l identified and reported to the NRC as required by 10 CFR 50.73, | |||
j despite newly acquired information that deenergizing an ESFAS i | |||
. | |||
sequencer required entry into the 1 hour limiting condition for | |||
l operation (Iro) action requirements of TS 3.0.3. In addition, the | |||
; possibility existed that the 140 for TS 3.0.3 (i.e. , 7 hours to hot | |||
. standby) were exceeded when the sequencers were previously | |||
i deenergized for maintenance and testing. This concern was based on | |||
(1) the lack of a specific TS for the sequencers, (2) the ' | |||
; operations Department historically linking the sequencer outages to | |||
! the emergency diesel generator (EDG) 140 of TS 3.8.1.1.b (78 hours | |||
, to hot standby), (3) a limited review of past maintenance work | |||
i orders (MW0s) indicated possible sequencer deenergiration; and | |||
' | |||
(4) comments by the engineering staff that the sequencers had been | |||
; | |||
previously deenergized. | |||
Discussion | |||
l There are two ESFAS sequencers for each unit--one for each 4.16- | |||
e kilovolt (kV) emergency bus. Each sequencer is activated by one of | |||
! two conditions, undervoltage (UV) on the associated emergency bus | |||
! or a respective train's safety injection (SI) signal. Upon receipt | |||
i of either or both of the initiating signals, each sequencer will | |||
j perform all or part of the following functions: | |||
' ' | |||
Start the associated EDG. | |||
I | |||
* i | |||
j Stop any test sequence in progress. | |||
LIMITED DISTRIBUTION - Not For Public Release | |||
- | |||
l' 24 | |||
. | |||
1 | |||
. | |||
= | |||
4 | |||
i | |||
- - - - - | |||
, . . _ _ _ _ _ - --__---_--__-___ | |||
_ . _ . _ _ _ _ _ _ . _ _ _ _ _ _ . _ ___ _ _ _ ._ _ . . _ _ _ _ _ . . . _ _ _ _ _. | |||
t | |||
'. e | |||
J | |||
! \ | |||
' LIMITED DISTRIBUTION - Nst For Public Roleano i | |||
' | |||
DRAFT - PREDECISIONAL INFORMATIDN | |||
; | |||
\ | |||
l | |||
* | |||
Strip the associated emergency bus of all loads (UV j | |||
i only). | |||
* | |||
close the associated EDG breaker (UV only). | |||
* | |||
[ Energize the associated train's engineered safety | |||
; | |||
features (EST) loads as determined by the initiating | |||
j signal. | |||
l Each ESFAS sequencer contains three levels of UV detection and | |||
; | |||
j | |||
system response, as well as the power supply for this UV circuitry. | |||
Four potential transformers monitor the emergency bus voltage for ! | |||
} these three levels of degraded bus voltage (Invel 1, 5 70 percent: l | |||
; Level 2, 5 86 percent; and 14 vel 3, 5 88.5 percent) and furnish an ; | |||
; analog signal to three sets of four bistables located in one of the | |||
4- | |||
. | |||
five sequencer cabinets. | |||
! | |||
Level _1 is the " loss of voltage" and Level 2 is the " degraded | |||
! | |||
i | |||
voltage" which is referred to in TS Table 3.3-2, Items 6.d, 8.a. | |||
and 8.b. As these TS items (applicable in Modes 1 through 4) do | |||
i | |||
not address the loss of all four channels in Level 1 or in Level 2 | |||
i | |||
(as would be the case when the sequencer is deenergized), TS 3.0.3 | |||
would apply if such a loss were to occur. It should be noted, | |||
i | |||
however, that if the sequencer were deenergized, it could not | |||
respond to a safety injection signal either. Therefore, there | |||
would be only one automatic safety injection actuation channel | |||
! (i.e., associated with the unit's unaffected sequencer) and Item | |||
i 1.b of TS Table 3.3-2 (6 hours to hot standby) would be the most | |||
l- limiting 140. 1 | |||
: | |||
'; Discussions with the operations manager, the assistant general i | |||
, | |||
manager-plant support, and system engineers for the ESFAS and ! | |||
i sequencers confirmed that the Operations Department historically ' | |||
2 | |||
linked the sequencer outages to the emergency diesel generator | |||
(EDG) 140 of TS 3.8.1.1.b (78 hours to hot standby) . Although the ) | |||
! | |||
; | |||
applicability | |||
had | |||
of TS Table 3.3-2 and TS 3.0.3 to sequencer outages l | |||
l been recently identified, past sequencer outages were not | |||
: reviewed. Therefore, with the assistance of the licensee, the ; | |||
i | |||
inspection team reviewed the completed MWOs which were performed on ' | |||
4 | |||
the sequencers on Units 1 and 2, as well as the related | |||
i | |||
1 | |||
Instrumentation and control (I&C) , Engineering, and Operations | |||
Department surveillance tests. | |||
- | |||
, | |||
) | |||
i | |||
, | |||
The review of completed MWOs did identify several instances where | |||
the work performed would most likely require the sequencers to be | |||
, | |||
deenergizedt however, the associated unit was found to have not | |||
. | |||
been in Modes 1, 2, 3, or 4 at the time the work was performed. | |||
. | |||
Somewhat = related to this concern, the review did identify two | |||
4 | |||
; | |||
- | |||
LIMITED DISTRIBUTION - Not For Public Release , | |||
j 25 | |||
! | |||
! | |||
. | |||
4 | |||
. | |||
- | |||
_ -_ _ _ _. _ _ __ _ _ _.__ _ _ _ _ __ _ __ _ _ __ ._ _ | |||
, . = | |||
; | |||
1 | |||
i | |||
. | |||
LIMITED DISTRIBUTION - Nat For Public R21ecco | |||
, | |||
DRAFT - PRIDECISIONAL INFORMATION | |||
. | |||
occurrences (March 4 and June 17, 1987) where the Unit 1 Train B | |||
l sequencer was inoperable during the change of sequencer controller | |||
4 | |||
card A (SI4T A4-3) . Specifically, when the controller card was | |||
j removed, both the automatic SI function and UV function for the | |||
; | |||
sequencer were rendered inoperable. Because the unit was in Mode | |||
i 3 (hot standby) during these two occurrences, the sequencers and | |||
the ESFAS were required to be operable per TS 3.3.2. However, the | |||
i associated 140 status sheets (1-87-354, dated March 4, 1987 and 1- | |||
I | |||
87-566, dated June 17, 1987) only recognized TS I40 3.8.1.1.b as | |||
being applicable to the outage. Despite the fact that 140s | |||
, | |||
associated with TS Table 3.3-2 (Item 1.b) and TS 3.0.3 were not | |||
- | |||
recognized, these TS were not violated since the system was | |||
j . restored within 30 minutes and 10 minutes, respectively, f1F | |||
i ' fditie , 2- ran unit rerrin:d in 5:t Ot:nry, pert:tility "adar | |||
_ | |||
4 | |||
j *^ 07 00.72 w 00.73 :: n;t r:';;ir:d [i.:., there t' : pr:r ! | |||
. | |||
r=A n<-+ 6 ihil: 1. 2 TS LOO (10 OFP 50.?2) ner we G. piani.-aken I | |||
j te hat utandhy er : :::Olt ;f e TO LOO (10 m 50. H ) F. 1 | |||
, | |||
i | |||
similar to the MWO review, the inspection team's review of related | |||
; | |||
I&C, Engineering, and Operations Department's surveillance tests | |||
l did not find any examples of the sequencers or the ESFAS being | |||
l deenergized in Modes 1 through 4. Completed 18-month ESFAS channel | |||
i calibrations, EDG tests, and ESTAS tests were verified as having | |||
i been done in Modes 5 and 6. Completed quarterly testing of the | |||
i ESFAS Auto SI K610 slave relay, which removed the automatic SI | |||
signal to the sequencer, were verified to be performed within time | |||
i limits allowed by TS 3.3.2. All other sequencer testing that used | |||
l installed test circuitry is automatically bypassed on an SI or UV | |||
: signal. | |||
4 | |||
i | |||
In addition to the inspection team's review of MWos and , | |||
l surveillance test procedures, the system engineers for the l | |||
i | |||
sequencers and ESFAS [as well as the nuclear steam supply system l | |||
; (NSSS) supervisor) were asked if they knew of any time in which the l | |||
4- sequencers were deenergized in Modes 1 through 4. None of these ' | |||
) | |||
engineers remembered any such occurrences. | |||
' | |||
A review of applicable operator treining material (System | |||
1 | |||
l | |||
. | |||
' Description 8b for Engineered Safety Features System Sequencers) | |||
revealed that there was no reference to ESFAS TS 3.3.2, just those | |||
for the diesel and other power sources and distributions (i.e., TS | |||
i 3.8.1.1, TS 3.8.3.2, TS 3.8.2.1, TS 3.8.3.1, and TS 3.8.3.2.). | |||
; | |||
This finding, along with the March 4 and June 17, 1987, occurrences | |||
l discussed above, indicates that the operations Department | |||
historically has not linked sequencer outages to the 140s of TS | |||
3.3.2 or TS 3.0.3. Nevertheless, discussions with the operations | |||
, | |||
~ manager and the licenced operators on shift indicated that although | |||
no written guidance or TS interpretation existed for the | |||
, | |||
, | |||
LIMITED DISTRIBUTION - Not For Public Release | |||
, 26 | |||
, | |||
! - | |||
, | |||
' | |||
- | |||
. _ . . . - | |||
_ _ _ _ _ . . _ _ _ __ . - _ _ _ _ __ ___ _ _ _ _ _ _ _ _ . _ _ _ - _ | |||
. | |||
: ! | |||
> | |||
.. | |||
< . | |||
; | |||
, | |||
LIMITED DISTRIBUTION - Not For Public Rslease l | |||
DRAFT - PREDECISIONAL INFORMATION l | |||
; | |||
; sequencers, the operations Department staff would currently ! | |||
consider all applicable TS requirements, including TS 3.3.2 and | |||
j 3.0.3. | |||
! Conclusion | |||
; The 140 actions of TS Table 3.3-2, "ESFAS Instrumentation," are ; | |||
' | |||
] applicable for determining the operability of ESFAS components; | |||
; | |||
' | |||
however,-if a load sequencer is not operable, the more restrictive i | |||
requirement of TS Table 3.3-2, TS 3.0.3, or the affected system Iro | |||
i should be considered. Although the EDG LCO of TS 3.8.1.1.b had ; | |||
:' | |||
been used for sequencer outages in t.he past, the allegation's ; | |||
concern of possibly exceeding the 140 for TS 3.0.3 when the : | |||
. | |||
sequencers were previously deenergized yM * not 5: ';11y , | |||
} c'2:t: .tiatad. loa!nR*1co. | |||
} Because there is no specific TS for the sequencers and considering , | |||
j (1) their unique interaction with numerous other systems and ; | |||
j equipment, and (2) the varying degrees in which related failures, ! | |||
i maintenance work, and surveillances can affect the sequencers' : | |||
j associated functions, the inspection team concluded that additie.31 ! | |||
guidance for the operators is warranted. Therefore, this issue l' | |||
l | |||
, | |||
will be followed as an inspector followup item pending further | |||
: | |||
review and evaluation and is identified as - | |||
I | |||
N-If 39- 6 | |||
; IFI 50-424/90-M and 50-425/90-xm-94, "Iack of Operator Guidance I | |||
1 | |||
concerning the Leo Actions Applicable During ESFAS Sequencer ' | |||
outages." | |||
1 | |||
:.- 2:11211!ty -' h-==~ v nine.1 r:eneratera | |||
{ | |||
i An allega n indicated that VEGP counted the number of starts | |||
e failures o e EDGs incorrectly and misrepresente is | |||
l information know in (1) a verbal presentation to C, (2) | |||
; a formal response to Region II confirmation o ction letter | |||
l (CAL), and (3) LER 90-00 , evision 0, issued owing the March | |||
j- 20, 1990, event involving fa es of the f1A. In addition, it | |||
j was alleged that VEGP attempte use the EDG reliability | |||
; issue with Revision 1, and delayed . -006, Revision 1, in order | |||
j to avoid drawing attention to ese inco et representations. | |||
1- | |||
i | |||
Discussion | |||
] | |||
The spection team reviewed the following: | |||
i | |||
i | |||
LIMITED DISTRIBUTION - Not For Public Release | |||
; 27 | |||
, | |||
e | |||
G | |||
w--, . --w vge ~ _ - | |||
_ _ - . . . . - - - . - - . - . - - . . . . . . . - . - ... - ~ . - . . . - . - . . . . - - | |||
1 | |||
l. . | |||
i . LIMITED DISTRIEUTION - Nat For Public R31eC03 | |||
DRAFT - PREDECISIONAL INFORMATION | |||
, | |||
!, 1) VEGP presentation in the Region II office ~ on April 9, 1990 | |||
; concerning the site area emergency event of March 20, 19 . | |||
his presentation is identified as Enclosure 2 to the Re on | |||
i meeting summary letter of May 14, 1990. / | |||
1 | |||
4 | |||
~2) VEG 1etter dated April 9, 1990, in response to the Region II | |||
i cont ation of action letter (CAL) dated March 23,'1990. } | |||
} ! | |||
j 3) LER 90-006, issued April 19, 1990, to report the site area | |||
emergen event of March 20, 1990. > | |||
i These documentsMnd the following procedures describe the EDG | |||
: operability.statu and the licensee's program for recording EDG | |||
! start information and the EDG surveillance test frequency i | |||
4 requirements: | |||
; | |||
\ | |||
* | |||
Procedure 550 8-C, " Diesel Start.Ing" l | |||
? | |||
' | |||
' | |||
Procedure 1314 -1, "EDG Operation for Maintenance | |||
Troubleshooting Maintenance Testing" | |||
^ | |||
* | |||
Procedure 14980-1, EDG Operability Test" i | |||
e | |||
l The licensee indicated in a tran | |||
\/arency used during the Region II | |||
l presentation that there were 18 s cessful starts on EDG f1A and 19 | |||
i | |||
' successful starts on EDG $15 tyeen the loss-of-offsite-power | |||
- | |||
event (March 20, 1990) and the pXesentation to Region II of | |||
April 9, 1990. The inspectiop' team r iewed the EDG start logs and | |||
j the detailed EDG start records complet during the performance of | |||
i Surveillance Procedures 13145-1 and 1498 -1. The inspection team's | |||
i review of these records in'dicated that th a were 31 EDG f1A and 29 | |||
: | |||
' | |||
EDG #1B attempted startpi Two of the EDG A and eight of the EDG | |||
f1B starts involved pr#blems or failures. EDG f1A there were a | |||
i total of 29 successful starts and on E 013 there were 21 | |||
i successful starts. However, there were s veral intermittent | |||
: problems or failurm/ s during the EDG f18 start tempts. Although | |||
! there were 29 6 sequential starts n EDG f1A, the | |||
; inspection team,7identified | |||
ccessful, that there were on1 12 successful, | |||
j sequential staits of EDG $15 during this time peri . | |||
i | |||
! TS 4.8.1.1. .a requires that each EDG be demonstrate operable in | |||
l accordane with the periodicity specified in TS Tabl 4 . 8-1 by | |||
l' Verifyl that the EDG starts and assumes rated fra ency and , | |||
voltage in accordance with the EDG surveillance test This | |||
;. surve lance test required a minimum run time of 1 hou at a | |||
l .desi ated load. The inspection team found that at the time the | |||
l pre entation to the NRC, the operability test of the EDGs had een | |||
s cessfully demonstrated two times. In addition, the EDGs ad | |||
l | |||
: LIMITED DISTRIBUTION - Not For Public Release | |||
: 28 | |||
j- | |||
i- | |||
. | |||
. | |||
n -. | |||
___ _ _ _ _ ..-_ _ _ . . _ _ _ _ _ _ _. _ __ _ _ _ _ __._. _ ._ | |||
i | |||
. .. | |||
. LIMITED DISTRIBUTION - Not For Public Ralesso * | |||
DRAFT - PREDECISIONAL INFORMATION | |||
i uccessfully passed four operability tests before Unit i entere | |||
j e 2. Therefore, the EDGs were reliable and operable before t e i | |||
j presentation. | |||
/ | |||
: | |||
- | |||
\ | |||
The WRC Region II Office was not verbally informed of the l | |||
j | |||
' | |||
incomp'lete information regarding the number of EDG starts until | |||
1 June 11 1990 (approximately 2 months after.the presentation). . | |||
j Although evision 1 of LER 90-006, dated June 29, 1990, correctly ! | |||
) identifiedsthe number of sequential, successful EDG starts from the i | |||
j and of the'saintenance test program (i.e., the first successful | |||
! operability st per TS 4. s . l .1. 2 a ) until the issuance of LER 90- | |||
i 006, Revision , dated April 19, 1990, this revision (June 29, | |||
j 1990) did not address the number of EDG starts that should have | |||
; been cited in th presentation, in the VEGP letter in response to | |||
the CAL, and in R 90-006, Revision O. The correct number of , | |||
j sequential, ' success ul starts for EDG #18 was 12 and not 19 as ! | |||
! indicated in the pres tation. Therefore, the NRC was not informed l | |||
of the correct informa ion in a timely manner. 1 | |||
: | |||
The information presente to the NRC did not coopletely describe | |||
. the problems and failures k at occurred with EDG $18. However, the ' | |||
i testimony indicates that t general manager's intention was to | |||
i demonstrate that the problem involving the immediate trip of EDGs | |||
identified during and follow gfthe March 20, 1990 event were | |||
corrected prior to Unit 1 start .- Therefore, a compliation of the | |||
; total number of successful sta' s (i.e., a start that did not | |||
s | |||
ortan factor in his presentation. | |||
i immediatelytrip)wasanimp/ | |||
l The testimony also indica d that e unit superinten: lent (Us) i | |||
- | |||
researched the EDG starti history fo the NRC presentation based | |||
; on a request from the ge ral manager. e general manager did not | |||
; ask the US to prepare a complete descri ion of the EDG starting | |||
i history. specifica11 ' the general manage requested a summary of | |||
l only the successfu starts--the informati concerning the EDG | |||
j problems and fallu s was not requested. In ddition, the Us used | |||
j the unit reactor rator logs instead of the E operating logs to | |||
; compile the EDG tarting history. The reactor perator logs did | |||
! not contain a etailed description of problems failures which | |||
! occurred dur g the EDG starts. The US did not ceive specific | |||
j guidance co erning the type.of EDG starts that he w requested to | |||
l | |||
summarise. In addition, the testimony indicated that the original | |||
, assumptigns and EDG $1B start information used in the esentation | |||
were alp 6 used in the VEGP response to the CAL, and in R 90-006 | |||
issuedApril 19, 1990. | |||
, i | |||
. | |||
Thef [nspection team's review of ' the Unit 1 EDG's reliabil and | |||
o rability status between March 21 and June 14, 1990, raise the | |||
11owing additional concern. The review was performed to ve fy | |||
l LIMITED DISTRIBUTION - Not For Public Release | |||
29 | |||
. | |||
t | |||
' | |||
4 | |||
' | |||
! . | |||
, | |||
! | |||
,. | |||
. , , . . . , . . , , , , _ . ._. _ . _ _ | |||
. - - . | |||
_ . _ _ _ . - -- _ _ _ | |||
, | |||
,. | |||
, | |||
LIMITED DISTRIBUTION - Not For Public R31ocS3 | |||
DRAFT - PREDECISIONAL INFORMATION | |||
t at all EDG failures were identified and classified as eit | |||
va id or non-valid and were reported to the NRC as required b TS | |||
r | |||
4.8. .1.3 and TS 6.8.2. The inspection team discovered tha the | |||
foll ing f ailures during starts of EDG f1B had not been clas ified | |||
as val d or non-valid and, consequently, had not been repofted to | |||
the NRC ursuant to TS 4.8.1.1.3 and TS 6.8.2. | |||
EDG S art Date Remarks | |||
/ | |||
1-90-13 3/22/90 EDG trfp, high- | |||
temperature lube oil. | |||
Ma i n 't e na nce | |||
troubleshooting test. | |||
/ | |||
1-90-134 3/23/90 EDG / trip, low jacket | |||
water pressure. | |||
M ,4 i nt a nance | |||
2 troubleshooting test. | |||
. | |||
1-90-136 3 24/90 EDG intentionally stopped | |||
due to alarmed condition, | |||
high jacket water | |||
temperature. Maintenance | |||
: | |||
troubleshooting test. | |||
1-90-157 5/23/ 0 EDG trip, high jacket | |||
water temperature | |||
M a i nt e na nce | |||
troubleshooting test. i | |||
< l | |||
4 | |||
1-90-160 5/23/90 END G trip, 1ow | |||
tutbocharger | |||
-161 o i' pressure. | |||
Main nance | |||
-162 troub e. shooting test. | |||
' | |||
' | |||
\ ' | |||
l | |||
1-90-164 5/23/90 EDG trip high jacket | |||
water | |||
-163 temperature. Maintenance | |||
troubleshoot g test. | |||
I | |||
These in .ction findings were discussed with the e ineering l | |||
support anager who agreed that these types of failures ave not ' | |||
been ported. The licensee committed to have all E start I | |||
, | |||
recor s reviewed for any unreported failures. | |||
Th inspection team also four.. that a violation -as previou ly | |||
i entified for the failure to report all EDG failures in Inspecti | |||
I | |||
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30 | |||
! | |||
l | |||
l | |||
. | |||
e | |||
l | |||
l | |||
. ~ - - . - . - . - - -_----..- _- -. - _ - . - -.. -- - - - . - - | |||
. . | |||
~ | |||
LIMITED DISTRIBUTION - Not For Public R310000 | |||
] DRAFT - PREDECISIONAL INFORMATION | |||
, Re rt 50-424/87-57 dated November 1987. Although the failur to | |||
, | |||
; | |||
repo all EDG failures is a violation of TS 3.8.1.1.3 | |||
6.8.2, the inspection team concluded that the failure | |||
d TS | |||
' s the | |||
result inadequate implementation of corrective a ions to | |||
j | |||
l | |||
prevent re urrence of a violation and, as such, is a vjdlation of | |||
- 10 CFR 50 Ap ndix 8, Criterion XVI, " Corrective Actiop," and will | |||
be followed a | |||
VIO 50-424/90-xx- , " Failure to Determine and Implement Adequate | |||
j Corrective Actions. , | |||
, | |||
/ | |||
j Conclusion | |||
1 | |||
/ | |||
/ l | |||
i The. allegation that VEGP i orrectly counted the number of starts | |||
l | |||
; and feilures of the EDGs a knowingly misrepresented the EDG ' | |||
. reliability in order to s1 cad the NRC was partially l | |||
. substantiated. On the basis of u sworn testimony and its review | |||
j j | |||
of EDG records, the. inspection te concluded that the Region II 1 | |||
, | |||
presentation was not intended to r resent a specific number of | |||
j successful valid tests as specified in G 1.108 and TS 4. 8.1.1.2a, l | |||
i | |||
but rather to describe the EDG maintenan test program and the EDG , | |||
! reliability status. Nevertheless, the i ction team concluded ! | |||
i | |||
; | |||
that the NRC was not informed of the incor et information until | |||
the NRC asked for it dh[ ring the inspection. l | |||
e lack of specific I | |||
; guidance concerning he EDG information desi d, coupled with | |||
: inadequate researc ! | |||
of the EDG starting histo , resulted in 1 | |||
providing incomp te and therefore inaccurate infotsation to the ] | |||
; | |||
NEC. The CAL r ponse and LER 90-006 were also inco ct because | |||
: they were bas on the IDG start information that was c iled for | |||
! the VEGP pr antation in the Region II Office. The inspec on teaa | |||
! concluded at the failure to provide accurate information o the | |||
] NRC was a violation of 10 CFR 50.9 requirements and wil be | |||
l follow as: . | |||
l VI 50-424/0-xx-05; 50-425/90-xx-05, " Failure to provide Accurate | |||
, | |||
r | |||
ornation to the NRC." | |||
, 7 6 y Air Quality of Emeraency Diesel Generator Startina Air System | |||
\ | |||
An allegation indicated that VEGP had no basis for its conclusions | |||
i regarding the air quality of the EDG starting air system and | |||
misrepresented the air quality in the licensee's written response , | |||
; to the CAL. | |||
I | |||
f Discussion | |||
i | |||
i | |||
The ir. pection team reviewed the maintenance records and deficiency | |||
; cards associated with Unit 1 EDG starting air system. The team i | |||
! | |||
LIMITED DISTRIBUTION - Not For Public Release | |||
i | |||
' 31 ' | |||
!. : | |||
! t | |||
' | |||
. | |||
' , | |||
9 | |||
* I | |||
e | |||
- _ _ _ _ _ _ _ - _ _ _ _ . _ . _ . , - , - - - . | |||
-. -- . | |||
. .. -- - - -. . _ ._ ._.__ -- - - - . | |||
q.- - | |||
, | |||
4 | |||
}. LIMITED DISTRIBUTION - Not For Public Release | |||
DRAFT - PREDECISIONAL INFORMATION , | |||
: | |||
, | |||
4 | |||
was established when preoperational tests were init | |||
on Unit 1 in November 1986. t | |||
: | |||
' this date, ' | |||
; | |||
; | |||
part of 1988,but' not on a scheduled frequency.During Dewpoint themeasurements | |||
latter w: | |||
! | |||
i established to measure the EDG starting air system The | |||
dewpoi{ | |||
! | |||
the | |||
current air drPM progran required checking the dewpoint monthly, cleanin ! | |||
' | |||
i | |||
i | |||
addition, yer condensing | |||
operating units,11882-1, | |||
Procedure and cleaning the fan motors. In | |||
i "Outside Area Rounds," i | |||
i dryers | |||
noisture. be blown down on a daily basis untilrequired that the E) | |||
i | |||
they were free of | |||
; | |||
operators blev The inspection team verified that the plant equipment , | |||
performance of their down the air systems on each shift during the | |||
rounds. | |||
! | |||
i | |||
! ; | |||
i | |||
A review of the Unit 1 EDG maintenance history records indicat e | |||
d | |||
. | |||
; | |||
that the majority | |||
specifications. of the devpoint | |||
There were instances, measurements taken were n | |||
withi i | |||
j | |||
i asasurements were above specifications.however, when the dewpoint i | |||
primarily | |||
instruments, attributed to problems with (1) These conditions were | |||
l | |||
extended pwriods (2) ofsystem | |||
time, andair dryers beingthe dewpoint measuring | |||
; | |||
system following maintenance. (3) repressurizing the EDG air start | |||
out of service for I | |||
i | |||
s | |||
The inspection team reviewed maintenance records associated an | |||
with | |||
internal inspection of the EDG air start system air receiver5- | |||
micron control _ air system filter inspection and replacement , | |||
the replacement of the dowpoint measuring instrument, with and | |||
; | |||
analyzer. an EG6 ; | |||
i | |||
* Following the loss of offsite power event of March 20 G | |||
1990, the control air system instrument lines were disconnected or | |||
,- | |||
f | |||
maintenance troubleshooting and functional tests of Calcon sensors | |||
; | |||
The system engineers associated with this work stated that no . | |||
i | |||
; evidence of internal noisture or corrosion was noted | |||
inspection and calibration of the calcon sensors or theair cortrol | |||
during | |||
; | |||
system instrument lines when this equipment was disconnected for | |||
. | |||
! | |||
maintenance troubleshooting and testing. | |||
j Conclusion - | |||
' | |||
!. | |||
: | |||
The inspection team concluded that the licensee did have an | |||
{' | |||
adequate basis to assess the quality of the EDG starting air | |||
system. , | |||
1 | |||
inspection | |||
addition, the of EDG air start system components a on. In | |||
for degr | |||
i PM program dewpoint readings have shown more | |||
; | |||
i | |||
The | |||
concerning allegation | |||
EDG air | |||
that | |||
start | |||
VEGP | |||
system | |||
did not have a ements | |||
aer.basis for th | |||
-4.i.uil-i A C #id *4 C D quality was not | |||
y -M4y | |||
I | |||
' ' | |||
LIMITED DISTRIBUTION 32 - Not For Public Release | |||
. | |||
; | |||
um * A INhgebm. | |||
yQWidLC. L m. eta & Guy as@v | |||
. | |||
i | |||
! | |||
- , . . _ _ | |||
. - _ - -. . - - - - . - - - - - _ - - - . . . . _ _ . - - . - - - .- - | |||
! c | |||
* | |||
j. - ! | |||
;. t | |||
j i' | |||
LIMITED DISTRIBUTION - Not For Public Release | |||
DRAFT - PREDECISIONAL INFORMATION | |||
; M | |||
y Reportability of Previous System Outages l | |||
f | |||
! | |||
An allegation indicated that VEGP failed to immediately notify the \< > | |||
{ | |||
j | |||
NRC as required by 10 CFR 50.72 when VEGP identified that both | |||
trains of the containment fan coolers (CFCs) had been previously | |||
inoperable at the same time on Unit 1. | |||
i | |||
j | |||
. | |||
I Discussion | |||
i | |||
i. | |||
I | |||
The inspection team's review of plant records indicated that this ! | |||
! condition occurred when EDG f1A was declared inoperable when tape | |||
(used when the EDG was being painted) was found on the EDG fuel | |||
j rack. The tape kept the fuel injector piston from moving and | |||
i injecting fuel into the EDG. With EDG f1A inoperable, the | |||
* | |||
. | |||
equipment associated with the Train A was also inoperable. In the | |||
process of investigating the installation of the tape, VEGP ! | |||
i; | |||
identified that this condition existed during a period when the | |||
Train B containment fan coolers were also in a degraded condition : | |||
j for maintenance. | |||
i | |||
' | |||
i | |||
During the performance of Surveillance. Procedure 14623-1, Train B | |||
! | |||
1 | |||
containment | |||
speed. 140 1-90-560 fan cooler (CFC) 1-1501-A7-003 failed to start in slow | |||
was initiated at 0115 hours on June 19, 1990, | |||
; | |||
J and maintenance on the CFC was initiated. The CFC was returned to | |||
j operable status on June 19,1990, at 1415 hours. Approximately 9 | |||
; | |||
hours later [on June 19,1990, at 2359 (Lco 1-90-562)), EDG f1A was | |||
i | |||
determined to be inoperable because the tape had been installed on | |||
i- the fuel rack. On July 17, 1990, VEGP issued LER 90-014 to | |||
j | |||
identify the previously unrecognized violation of the 140 in | |||
; accordance with 10 CFR 50.73. | |||
' | |||
, Conclusion | |||
! | |||
Based upon the fact that VEGP did not become aware that both trains | |||
, | |||
of CFCs were simultaneously inoperable until after the Train B CFC | |||
! | |||
j fan had been returned to service, the immediate notification | |||
requirements of 10 CFR 50.72 were not applicable. The allegation | |||
, that previously | |||
the VEGP failed to immediately | |||
degraded c notify the NRC upon discovery of | |||
; e , - ,ondition> . | |||
of the CFCs was not .Se44y | |||
j | |||
g.1 W Intimidation of Plant Review Board (PRB) Members | |||
i | |||
i | |||
f An allegation indicated that Plant Review Board (PRB) members were | |||
allegedl | |||
j meeting.y intimidated and pressured by the general manager in a PRB | |||
The meeting occurred in February 1990, to determine the | |||
: | |||
} , | |||
j LIMITED DISTRIBUTION - Not For Public Release | |||
j. - | |||
33 | |||
i | |||
i | |||
!- | |||
! . | |||
l | |||
. | |||
l | |||
1 | |||
_. . _ . _ . . _ _ . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ . _ _ | |||
. | |||
.. . | |||
. | |||
LIMITED DISTRIBUTION - Not For Public R21enSO | |||
DRAFT - PREDECISIONAL INFORMATION | |||
acceptability of the safety analysis for the installation of the | |||
FAVA microfiltration system. | |||
Discussion | |||
T.i j | |||
k | |||
As discussed in Section ht" of this inspection report, several , | |||
! | |||
' | |||
safety evaluations were performed for the installation of a | |||
temporary modification which installed the FAVA microfiltration | |||
i system. Discussions with PRB members indicated that during the | |||
t review of these safety evaluations, various PRB members had | |||
1 expressed reservations on several occasions concerning the | |||
4 | |||
acceptability of the installation of the FAVA system. | |||
! | |||
.' Despite these reservations, the inspection team's review of the PRB | |||
: Meeting minutes associated with this temporary modification | |||
j | |||
identified few instances of the PRB members documenting their | |||
i dissenting opinions. Specifically, PRB meeting 90-15 (dated | |||
February 8, 1990) documented one PRB member's negative vote and | |||
' | |||
i dissenting opinions regarding the acceptability of exempting the | |||
temporary modification from regu'.atory requirements and the | |||
, adequacy of the system's safety evaluation. PRS Meeting 90-28 | |||
. (dated March 1, 1990) indicated that information and issues | |||
regarding the FAVA system's safety analysis were presented to the | |||
j PRB and that the general manager solicited written comments and | |||
! questions from other members for resolution. The only other | |||
l example was in PRB meeting 90-32 (dated March 6, 1990) which | |||
!- identified a dissenting opinion related to the acceptability of | |||
j votina on the FAVA system installation when the PRB member who ; | |||
: raised the initial questions and concerns on the operation of the | |||
i FAVA system was not present. | |||
! Discussions with the PRB members indicated that during the various | |||
: | |||
PRB meetings concerning the installation of the FAVA system, the ; | |||
i PRB members felt intimidated and pressured by the presence of the ' | |||
l- general manager at the PRB meeting. The sworn testimony confirmed | |||
4 | |||
that on one occasion an alternate voting member felt intimidated ; | |||
; and feared retribution or retaliation because the general manager i | |||
j was present at the meeting and the PRB member knew the general 1 | |||
j. manager wanted to have the temporary modification approved. ; | |||
j However, the testimony also indicated that the.PRB member did not ' | |||
a | |||
alter his vote and felt comfortable with how he had voted. In | |||
l addition, the PRB member was not aware of any occasions on which he | |||
or any other PRB member had succumbed to intimidation or feared ; | |||
i | |||
! retribution. | |||
! | |||
' | |||
The incpection team verified that the general manager was informed l | |||
i | |||
following this meeting that several PRB members viewed his presence | |||
; as intimidating. As a result, on March 1, 1990, the general | |||
, | |||
! | |||
LIMITED DISTRIBUTION - Not For Public Release l | |||
l 34 ! | |||
. | |||
L | |||
, | |||
- | |||
I | |||
i | |||
I | |||
- - - - - - _ _ _ . - . - - . . - - . . - . - - - _ - - . - - . - . - . - - - - - . | |||
. . . | |||
. l | |||
! | |||
, | |||
LIMITED DISTRIBUTION - Not For Public Release | |||
DRAFT '- PREDECISIONAL INFORMATION | |||
manager set with all PRB members to reiterate the member's duties | |||
and responsibilities. | |||
He specifically told the members that his | |||
presence at PRB meetings must not | |||
influence them and that ! | |||
alternates should be | |||
responsibility. Heselected who would feel comfortable with this | |||
also addressed i | |||
the difference between | |||
and their respective methods for resolution. or quality concerns, | |||
professional differences of opinion and safety | |||
conclusion , | |||
; | |||
The inspection | |||
felt intimidated | |||
was present at the andPRB team | |||
feared retribution | |||
meeting. concludedbecause the that general in manager | |||
on* case a PRl | |||
However, this member 6ala nor W | |||
change his vote in response to this pressure and the general | |||
manager met with the PRB to allay fears. Based on the testimony, | |||
the inspection team concluded that retribution did not occur. i | |||
Nevertheless, this confirmed event and the absence of dissenting ' | |||
opinions in the PRB meeting minutes indicate that there was a ' | |||
potential for an adverse affect on open discussions at the meeting, t | |||
The licensee needs to ensure that PRB members freel | |||
express their technical opinions and safety concerns.y and openly | |||
K Personnel Accountability | |||
As a result of several comments and questions by the licenced | |||
operators | |||
to rate theto the inspection team, the team reviewed the method used | |||
supervisors. performance of the shift superintendents and unit shift | |||
Discussion | |||
The o | |||
rations manager stated that the shift superintendents (SSs) | |||
" | |||
e SSs re ed to su int ndent | |||
i s and a | |||
US personally prepared the performance appraisals of the 8 s. | |||
; | |||
i The personnel accountability system, first used in 1989, was a pay- | |||
for-performance methodology. Annual pay increases and e percentage | |||
i of | |||
in the Operations Department | |||
accountability categories. bonus were dependent on their ratings | |||
, | |||
i | |||
subdivided into performance categories.Each accountability Most of the performance category was ! | |||
categories vern based upon group performance. | |||
. | |||
' | |||
l | |||
eliminated, any differential in pay will Once these are i | |||
; result from eight | |||
t | |||
performance categories. Implementation of the plan in 1989 could | |||
i result in | |||
superintendent. up to an $8,000-a-year difference 'n bcnus pay to a shift | |||
weights are: The performance categories and their relative | |||
: | |||
, LIMITED DISTRIBUTION - Not For Public Release | |||
35 | |||
! | |||
l | |||
. | |||
. | |||
. | |||
- | |||
_ __ .-_ .- - - - ---- - --^ - | |||
: | |||
. . . . , | |||
a* | |||
LIMITED DISTRIBUTION - Not For Public Release | |||
DRAFT - PREDECISIONAL INFORMATION | |||
. * | |||
Personnel safety 4.1% | |||
i | |||
' | |||
. | |||
Regulatory compliance 10.2% | |||
. | |||
: | |||
* | |||
ESFAS actuation 12.2% } | |||
* | |||
I Reactor trips 10.2% | |||
! | |||
' | |||
* MWO performance 4.1% | |||
' | |||
. | |||
Special projects a.2% ' | |||
= | |||
Personnel development 30.6% | |||
l . | |||
Training 20.4% | |||
, | |||
i | |||
{ Therefore, 51 percent will be associated with personnel development | |||
] | |||
and training and 32.6 percent will be associated with the number of | |||
; LERs, and violations (i.e. , regulatory compliance (10.2 percent), ; | |||
. | |||
ESFAS actuation (12.2 percent) and reactor trips (10.2 percent)]. ' | |||
Conclusion | |||
' | |||
The inspection team concluded that there was a | |||
t | |||
potential | |||
' | |||
, | |||
disincentive for identifying items which may result in LERs or | |||
violations. | |||
' | |||
In addition, the inspection team concluded that the | |||
j operations manager | |||
information to the inspection provided incorrect | |||
team. or inadequately researched | |||
! | |||
i | |||
; | |||
The inaccurate information ) | |||
concerned whether the operations manager personally performed the | |||
a | |||
: | |||
performance appraisals of shift superintendents. The information i | |||
: -was not very important because the inspection team did not use the 3 | |||
j informationteam | |||
inspection as the basis forthat | |||
concluded a significant | |||
this failure inspection finding. The { | |||
- | |||
to provide accurate ] | |||
i information was an example of a violation of the 10CFR 50.9 | |||
{ | |||
requirements | |||
followed as: to provide accurate information to the NRC and will be | |||
' 14-1L- Ig-12. | |||
, | |||
VIO 50-424/90-aoeHPJ; 50-425/90.xx-65, " Failure to Provide Accurate | |||
: Information to the NRC." | |||
' | |||
j 3.0 EXIT INTERVIEWS | |||
1 | |||
' | |||
The inspection scope and findings were summarized on August 17, | |||
i | |||
1990, with those persons indicated in Appendix 2. The inspection | |||
team described | |||
inspection results.the areas inspected and discussed in detail the | |||
The licensee made numerous | |||
, | |||
comments. dissenting | |||
i | |||
materials provided to or reviewedThe licensee did not identify as proprietary any o | |||
i inspection. by the inspector during this | |||
: | |||
, | |||
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- | |||
LIMITED DISTRIBUTION - Not For Public Release | |||
DRAFT - PREDECISIONAL INFORMATION | |||
APPENDIX 1 | |||
LIST OF TRANSCRIBED INTERVIEWS | |||
DATE TIME PERSON | |||
, | |||
8/14/90 904 hours George Bockhold | |||
911 hours Jim Swartzwelder | |||
1023 hours Harvey Handfinger | |||
1026 hours Bill Diehl | |||
1109 hours Mike Horton | |||
1335 hours Mike Chance | |||
1136 hours Jimmy Paul cash | |||
1338 hours Dudley Carter | |||
1529 hours Bruce Kaplan | |||
1625 hours Greg Lee | |||
1800 hours Jeff Gasser | |||
8/15/90 906 hours Allen Mosbaugh | |||
937 hours Ernie Thornton | |||
1009 hours John Gwin | |||
1048 hours Steve Waldrup | |||
1335 hours Jerry Bowden | |||
1452 hours John williams | |||
1637 hours Carolyn Tynan | |||
1730 hours John Williams l | |||
l | |||
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g 44 9 | |||
' | |||
LIMITED DISTRIBUTION - Not For Public Release l | |||
DRAFT - PREDECISIONAL INFORMATION I | |||
APPENDIX 2 | |||
PERSONS CONTACTED | |||
Licensee Employees | |||
*J. Aufdenkampe, Manager Technical Support | |||
*G. Bockhold, Jr. , General Manager Nuclear Plant | |||
*D. Carter, Shift Superintendent | |||
J. Bowden, Work Planning , | |||
J. Cash, Unit Superintendent l | |||
M. Chance, Senior Engineer, Engineering Support , | |||
*S. Chesnut, Technical Support i | |||
C. Coursey, Mair.cenance Superintendent l | |||
W. Diehl, Shif t Supervisor, Operations | |||
Frederick, Safety Audit and Engineering Group Supervisor | |||
, | |||
*G. 1 | |||
J. Gasser, Shift Superintendent, Operations | |||
*L. Glenn, Manager. - Corporate Concerns | |||
*D. Gustafson, Maintenance Engineering Supervisor i | |||
J. Gwin, Corporate Systen Engineer | |||
*H. Handfinger, Manager Maintenance | |||
*K. Holmes, Manager Training and Emergency Preparedness ! | |||
*M. Horton, Manager Engineering Support | |||
. | |||
, | |||
B. Kaplan, Senior Engineer, Engineering Support | |||
G. Lee, Plant Engineering Supervisor, Operations | |||
*R. LeGrand, Manager Health Physics and Chemistry | |||
W. Lyons, Quality Concerns Coordinator ; | |||
*G. McCarley, Independent safety Engineering Group Supervisor | |||
*C. McCoy, Vice-President, Georgia Power Company | |||
*R. Mcdonald, Executive Vice-President, Georgia Power Company l | |||
*D. Moncus, Outage and Planning ; | |||
*A. Mosbaugh, VEGP Staff ' | |||
R. Odom, Nuclear Safety and Compliance Manager l | |||
*A. Rickman, Senior Engineer - Nuclear Safety and Compliance i | |||
*L. Russell, Independent safety Engineering Group, SONOPCO | |||
*M. Shelbani, Senior Engineer ! | |||
*C. Stinespring, Manager Plant Administration | |||
*S. Swanson, Outage and Planning Supervisor ; | |||
*J. Swartzwelder, Manager Operations - | |||
E. Thorton, Shif t Supervisor, Operations I | |||
*E. Toupin, Oglethorpe Power Corporation . | |||
C. Tynan, PRB Secretary i | |||
S. Waldrup, Planning and Scheduling Supervisor | |||
J. Williams, Shift Superintendent, Operations , | |||
* Attended exit interview, August 16, 1990. ; | |||
! | |||
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38 | |||
j. l | |||
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._..m , - , ., . , _ , , . . . _ _ ___..___._______________# | |||
._. -. - - . -- - - . . _ . - _ . - - - . _ - - . _ _ . . ___ | |||
, s. , | |||
, | |||
LIMITED DISTRIBUTION - Not For Public Release | |||
DRAFT - PREDECISIONAL INFORMATION | |||
APPENDIX 2 | |||
PERSONS CONTACTED (continued) | |||
! NRC Employees Who Attended Exit Interview | |||
- | |||
R. Aiello, Resident Inspector - Vogtle | |||
; | |||
B. Bonser, Senior Resident Inspector - Vogtle | |||
M. Branch, Senior Resident Inspector - Watts Bar | |||
: | |||
R. Carroll, Project Engineer - RIIK. Brockman, Chief, Reacto | |||
i | |||
N. Huneauller, Reactor Engineer - NRRL. Carner, Senior R | |||
0. Matthews, | |||
> | |||
Project Director - NRR | |||
J. Milhoan, Deputy Regional Administrator - RII | |||
R. Starkey, Resident Inspector - VogtleL. Reyes, Directo | |||
P. Taylor, Reactor Inspector - RII | |||
M. Thomas, Reactor Inspector - RII | |||
, | |||
C. VanDenburgh, Section Chief - NRR | |||
J. Wilcox, Operation Engineer - NRR | |||
e | |||
l | |||
; | |||
! | |||
: | |||
. | |||
i | |||
1 | |||
4 | |||
: | |||
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, | |||
39 | |||
. | |||
. | |||
* ' ' | |||
LIMITED DISTRIBUTION .Not For Public R21onso | |||
- DRAFT - PREDECISIONAL INFORMATION | |||
APPENDIX 3 | |||
LIST OF ACRONYMS i | |||
AOP Abnormal Operating Procedure | |||
ARB. Alternate radwaste building | |||
ASME' American Society of Mechanical Engineers | |||
CAL Confirmation of action letter i | |||
CFC Containment Fan Cooler j | |||
CFR Code of Federal Regulations l | |||
CIV containment isolation valve | |||
DC Deficiency card | |||
DRP Division of Reactor Projects | |||
EDG Emergency diesel generator i | |||
Electric Power Research Institute | |||
' | |||
EPRI | |||
ESF Engineered safety features | |||
ESFAS Engineered safety features actuation system | |||
TSAR Final Safety Analysis Report ; | |||
NUT Holdup tank | |||
I&C Instrumentation and controls | |||
IFI Inspector follovup iten | |||
IST Inservice test | |||
kV Kilovolt | |||
LCO Limiting condition for operation | |||
LER Licensee Event Report | |||
NWO Maintenance work order | |||
NRC Nuclear Regulatory Commission | |||
NRR Nuclear Reactor Regulation | |||
NSCW Nuclear service cooling water | |||
NSSS Nuclear steam supply system | |||
OI Office of Investigations | |||
PM Preventative maintenance | |||
PRB Plant Review Board | |||
psig Pounds per square inch gauge | |||
PVC Polyvinyl chloride | |||
QA Quality Assurance | |||
RII Region II Office | |||
: RCS Reactor coolant system | |||
l REA Request for engineering assistance | |||
; | |||
RG Regulatory Guide , | |||
' | |||
l RHR Residual heat removal | |||
SER Safety Evaluation Report | |||
j SI safety injection | |||
i SONOPCO Southern Nuclear Operating Company | |||
; SRM Source range monitor | |||
. SS shift superintendent ' | |||
; | |||
SSS Shift support supervisor | |||
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i 40 | |||
. | |||
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; | |||
* | |||
i | |||
_ a | |||
. - .. - . . - | |||
). . | |||
*~ ' | |||
LIMITED DISTRIBUTION - Not For Public Release | |||
DRAPT - PREDECISIONAL INFORMATION | |||
APPENDIX 3 ' | |||
LIST OF ACRONYMS (continued) | |||
STS Surveillance task sheet | |||
TCP Temporary change to procedure | |||
TS Technical Specification | |||
USS Unit shift superintendent | |||
UV Undervoltage | |||
VEGP Vogtle Electric Generati!.g Plant | |||
VIO Violation | |||
, | |||
i | |||
i | |||
. | |||
LIMITED DISTRIBUTION - Not For Public Release | |||
< | |||
41 | |||
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}} |
Latest revision as of 14:05, 21 August 2022
ML20129F418 | |
Person / Time | |
---|---|
Site: | Vogtle |
Issue date: | 07/23/1991 |
From: | Reyes L NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
To: | Vandenburgh C Office of Nuclear Reactor Regulation |
Shared Package | |
ML20129F106 | List:
|
References | |
FOIA-94-208 NUDOCS 9610040144 | |
Download: ML20129F418 (56) | |
See also: IR 05000424/1990019
Text
_ __
UNITED STATES
. [pm neo 'o NUCLEAR REGULATCRY COMMISSION
. [ , CE! ION 11
- y ,P 101 MARIETTA STREET, N.W.
, s ATLANTA, GEOR0dA 30323
'+,.....
JUL 2 31991
MEMORANN N F0P, Chris A. VanDenburgh, Chief, Reactive Inspection Section 2
Vendor Inspection Branch
Division of Reactor Inspections and Safeguards
FROM: Luis A. Reyes, Director e
Division of Reactor Projects
SUBJECT: V0GTLE SPECIAL TEAM INSPECTION - ALLEGATION FOLLOWUP TEAM
DRAFT INSPECTION REPORT (INSPECTION REPORT NOS. 50-424/90-XX
AND50-425/90-XX)
This memorandum refers to the special inspection conducted on August 6
through 17, 1990, at the Vogtle Electric Generating Plant (VEGP). This
'
inspection involved a review of several allegations regarding the safe
operation of VEGP and the review of operational activities generally related
to the allegations. As discussed in the inspection plan, the inspection was
performed by two separate teams--an operational followup and an allegation
,
followup team.
As decided in a meeting held in Nuclear Regulatory Commission (NRC) head-
quarters on September 26, 1990, the allegation followup team's findings and
conclusions was not included in Inspection Report 50-424/90-19;
50-425/90-19. This information was to be withheld pending the completion of
an Office of Investigation review of the allegations and the inspection
team's conclusions. On January 11, 1991, Inspection Report 50-424,425/90-19
was issued which included the operational followup team findings. The
remaining issues from the allegation followup team were then left in
Inspection Report 90-XX, pending the completion of Ois' review of the
'
allegations.
On July 9,1991, a meeting was held in Region II, with members of Region
II-DRP, 01, and NRR-PD3-2 and Regional management. It was determined to j
,
-
issue the remainder of the 50-424,425/90-19 report, except for the following i
issues: 1) 12.3 Missed Containment Isolation Valve Surveillance; 2) 12.4
Mode Change With Inoperable Source Range Monitor Nuclear Instrument; 3) 1
2.7 Reliability of Emergency Diesel Generators and their corresponding parts
to the Notice of Violations.
This memorandum forwards a marked up copy of Inspection Report 50-424,
425!90-19, Supplement 1, which documents the inspection team's review and
conclusions regarding the allegations as of the time of the inspection exit
meeting on August 17, 1990 The report has already been reviewed by the
'
.
Office of Investigation in Region II for information that clight compromise
their on going investigations. The information that was considered
l
pertinent to these investigations will not be included in the issued report.
-
l \
9610040144 960827 l
COLAPIN94-200 PDR i
!
.. .- _ . - . . - . . . . . .- - .. - - _- . - . - - - . - . - . . . _ - -
. _
. - . . ,
!
' !
'
- " I
..
Chris A. VanDenburgh
.
2 JUL 2 31991 l
!
i
If you have any questions concerning this issue, please contact P. Skinner !
at Ext.16299 or S. Vias at Ext.15350. :
'i
'
~/ 4 l
'
Luis A. R
!
Enclosures
~1. Draft Notice of Violation i
2. Draft -Inspection Report '
50-424,425/90-19 Supplement I
cc w/encis: !
L. Robinson 01. i
D. Hood, NRR, PD3-2~ t
s.445
&.%nd
t. %e 5
6. Jul
l
,
I
l
I
___._._________-___:
. .. _ _ .. - -- - . . . - - - _~. -- - - - - . _ -
- ';
, ioi maasts ta sie<tti. n.
4 ;; e anc.mA.etonc A 3o323
.
- ' . M%II G;
- 1
i Docket Nos. 50-424 and 50-425 J
'
i
i Georgia Power Company
- ATTN: Nr. W. G. Hairston, III i
'
4 Senior Vice President - .
i
j Nuclear operations q L
)
<
P.O. Box 1295 y '
) Birmingham, AL 35201
Gentlemen:
SUBJECT: VOGTLE SPECIAL TEAM INSPECTION AND NOTICE OF VIDIATION
1 (NRC INSPECTION REPORT 3
NOS. 50-424/90-19 AND
50-425/90-1gg SuppleAw
- This refers to the inspection conducted by an NRC Special p !
j
!
Inspection Team
included a
on August 6 through 17, 1990.Jr Tne inspem. ion .Ag'
review of activities authorized for your Vogtle
i
facility. At the conclusion of the inspection, thePffindings were
3
i
i
discussed with those members of your staff identified in the
j
i
enclosed inspection report. }[
- Areas examined during the inspection are identified in the report.
! Within these areas, the inspection consisted of selective
examinations of procedures and representative records, interviews
j. with personnel, and observation of activities in progress.
. Based on the results of this inspection, certain of your activities
.
appeared to be in violation of NRC requirements, as specified in
j the enclosed Notice of Violation (Notice). i
i
-1^3 *hatthe inspection concluded that the facility was opera
_
- a safe mann..- Q dance with the requirements perating
l license, we are conc =..:f that there e veral operational !
- policies and programs whers we ___ - laantified. As part of i
, your response to the ons identified n sed Notice,
- you are a sted to address each of the weaknesses ___A
l ion summary.
!
! You are required to respond to this letter and Notice and should ,
follow the instructions specified in the enclosed Notice when !
preparing your response to the violations. In your response, you 1
l should document the specific actions taken and any additional
i actions you plan to prevent recurrence. After reviewing your
'
response to this Notice, including your proposed corrective actions
and the results of future inspections, the NRC will determine
- whether further NRC enforcement action is necessary to ensure
compliance with NRC regulatory requirements. .
-
.
Q.4 4t g f & LeM-e t % w e.e U An, 491. d* k, & ~?
-
w k w'U. J 4 m e
- A
y py a 9
S . = --
Wx A,4 d
ra. Ah..j N
A
w . % .*r q t 4 A '== ,4 M
,
--
L Wu u,< 4 a m, ,a 1 A. /
i
a
._-
2
M II E
coorgio Pov3r CcIpany
'
4
a
E d!*ionally, you should respond to each of the o esses are
(The
weaknessesMfied within the report. ary.) The response
specifically annotated-in .the InspectioMhe s3gnificance of the weaknesses
.
should address your analysis at these operat tices do not ,
and your actions toof non-compliance or reduce the marg n 7:'ev ^
evolve int
p ant.
.
'
In accordance with section 2.790 of the NRC's " Rules of Practice,"
a copy of this letter and its enclosures will be placed in the NRC
Public Document Room. r
The responses directed by this letter and the enclosed
and Budget as required by the Paperwork Reduction Act of 1980,
Pub. L. No. 96. 511.
Should you have any questions concerning this letter, please
4 contact us.
sincerely,
0
>
i
-
>
ne r
' Regional Administrator f
<
,
Region II
.
I
l
Enclosures:
1. Notice of Violation
2. Inspection Report 50-424/90-191 l
50-425/90-19 % (pl* * d 1
l
I
l
,
9d b
.
df f
YS
7
1
.
-
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W he 'l + 1 9/ hi ,/ jv
-
,
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,
,
s. . . . ..n.
LIMITED DISTRIBUTION - Not For Public Ralesco h, '
DRAFT - PREDECISIONAL INFORMATION E,N,";,'" ,
,-
May 9, 1991 P[ %[
-> .
.
,,
MEMO DUM FOR: Luis A. Reyes, Director g:~ y .i
Division of Reactor Projects fq ',* : ~
-
Region II .6.'N ', ' '
FROM: Chris A. VanDenburgh, Chief NY '- " '-4'.:..T.1 + '-
Reactive Inspection Section - 2 [5EF.('-j ,y..
Vendor Inspection Branch ;
Division of Reactor Inspection and i
'
Safeguards
SUIL7ECT: VOGTLE ECIAL TEAM INSPECTION - ALLEG TION FOLLOWUP TEAM ;
DRAFT SPECTION REPORT (INSPE ION REPORT NOS. !
50-424/90 x AND 50-425/90-xx) l
This memorandum refer to the special spection conducted on
August 6 through 17, 19 , at the Vogtle lectric Generating Plant .
(VEGP). This inspection nvolved a rev ew of several allegations
regarding the safe operati of VEGP a d the review of operational ;
i
activities generally relate to the legations. As discussed in
the inspection plan, the ins ction was performed by two separate
teams--an operational followup nd n allegation followup team. At
the conclusion of the inspect , all of the inspection team's ,
conclusions with respect to the erations and allegation followup l
were discussed with the me s GP's staff identified in the
I
enclosed draft inspection re rt.
As decided in a meeting hel in Nuclea egulatory Commission (NRC)
headquarters on September 26, 1990, the llegation followup team's
findings and conclusio have not bee included in Inspection
Report 424/90-19; 50-4 /90-19. This info ation has been withheld
pending the completi of an office of Inve igation review of the
allegations and the spection team's conclus ns. This memorandum ,
'
forwards a draft spection report (50-424/ -xx; 50-425/90-xx)
s
'
which documents e inspection team's revie and conclusions
regarding the a egations as of the time of th inspection exit
meeting on Au t 17, 1990.
. The areas e amined during the inspection are iden fled in the -
inspection eport. As discussed in Inspection Report -424/90-19;
50-425/90 9, the inspection team concluded that the f ility was
, safely rated. However, the inspection identifie several '
i instan s in which the VEGP was not operated in accordance ith the ,
inten of the Technical Specifications. In additio the
- insp ction identified several potential weaknesses i the
'
fa lities' operational r licies and practicc..
i
LIMITED DISTRIBUTION - Not For Public Release i
I
- ,
l
!
1
.
J
i .
j
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!
i
.- - .--. -.
.-
- . .- - . - . . .- - -- - _. - - - - ._ . - . _ - - .
b
, .
LIMITED DISTRIBUTION - Not For Public Release
DRAFT - PREDECISIONAL INFORMATION
i
Lui A. Reyes -2- '
The ins'pection team's review of the allegations identified severa
additio 1 weaknesses in these operational policies and practice .
These ar identified in the inspection summary of the enci ed ,
'
draft insp ction report.
Based on the t artain
activities app,esults eared toof this inspection
be in violationofof theNRC allegations,
require nts, as
specified in t e enclosed draft Notice of Violation (Notice).
These violations re important because they indicate ( a failure
to implement the r cations and
-
administrative proc,equirements
9 dures, and (2) of the
theTechnical
failure to Speci
pr vide accurate
information to the .
As part of the response to the violations /dentified in the
~
'
enclosed notice, VEGP should also be requeste to address each of
the concerns listed in t e inspection summa .
t
!
!
Enclosures:
1. Draft Notice of Violation
2. Draft Inspection Report 50-434/90-xx; 50-425/90-xx
/
cc:
BKGrimes
EWBrach
.
d
I
f
l LINITED DISTRIBUTION - Not For Public Release
i
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_ _ _ _ _ _ _ _ - . . _ . .
_.
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LIMITED DISTRIBUTION - Not For Public RalGG00
DRAFT - PREDECISIONAL INFORMATICN
,
N >
l
l
l
NRR/DRIS RII/DRP RII/DRP RII/DRP
JWilcox* RAlello* RStarkey* MBranch*
9/ /90 8/31/9 8/31/90 8/31/90
1
I
RII/DRP RII RS NRR/DLPQ RJI/DRS
I4arner* MThomas* NHuneauller* ylore
9/27/90 /31/90 8/31/90 8/ 1/90 ;
1
i
RII/DRP NRR/DRIS i
'
RCarroll* CVanDenburgh '
8/31/90 9/ /90 l
l
- Se previous concurrences
'
LIMITED DISTRIBUTION - Not For Public Release
.
- - - - .- - - _ - - . . . - . . . . . - - . - . . . . _ _ - _ __ _ - _ . _ _ .
!
.
.
LIMITED DISTRIBUTION - Not For Public R31easo
DRAFT - PREDECISIONAL INFORMATION
ENCLOSURE 1 !
,
NOTICE OF VIOIATION
<
l Georgia Power Company Docket Nos. 50-424 and 50-425
Vogtle Electric Generating Plant License Nos. NPF-68 and NPF-81 l
3 Units 1 and 2 l
'
,
l
l During an NRC inspection conducted on August 6 through 17, 1990, ,
violations of NRC requirements were identified. In accordance with l
- the " General Statement of Policy and Procedure for NRC Enforcement i
! Actions," 10 CFR Part 2, Appendix C (1990), the violations are l
!
i
listed below. '
!
l
l
"
A. 10 CFR Part 50.9, " Completeness and Accuracy of Information,"
requires that info mation provided to the NRC by a licensee
- shall be complete and accurate in all material respects.
I Contrary to the above, the licensee provided g separate
curate
, information to the inspection team on 4heee
1
occasions. Although the information was provided in unsworn,
1 oral statements, the information provided was significant to
the licensing process. The information was provided by
l licensed operators, supervisors and management concerning
i information which was within their specific responsibilities. 1 i
l The d4ve examples were as follows. (50-424/90-eese-95; 50- l
'
! 90-eas-99) li - I'L l
l
'
IV'2-
1. Containment Isolation Valves: During a Unit 2
surveillance procedure, the unit shift supervisor (USS)
,
'
i
stated, and the operations manager later confirmed, that
'
j the containment isolation valves for the hydrogen monitor
3 system were allowed to be opened without entering the
3 limiting condition for operation (Ico) action
- requirements for Technical specification (Ts) 3.6.3
because the valves received an automatic isolation
.3 signal. The inspection identified that these containment
] isolation valves were remotely-operated, manual valves
without automatic isolation signals. (Discussed in
Section 2.2.1.1 of Inspection Report 50-424/90-19; 50-
425/90-19)
4 2. Snubber Reduction: The operations manager stated that,
! after the second Unit i refueling outage (1R2), the
!
modifications to tt:e snubbers were done in conjunction !
'
.
LIMITED DISTRIBUTION - Not For Public Release 1
1
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_- . - - - - -- -- _. - -
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3g personnel Accountabiliev: The operations manager stated that
the shift superintendents (SSs) reported directly to the
operations manager and that he personally prepared their
performance appraisals. The inspection identified that the
sss reported to the unit superintendent (Us), and that the US
1 personally prepared the performance appraisals of the Sss. j
- (Discussed ;,n section 2.Af of this inspection report)
- O ,
4 y) Ts 3. 0. 3 Actions: The unit superintendent indicated that
- there were no Operations Department actions which were i
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anticipated or required within the first three hours of
entering the action statement of TS 3.0.3. The inspection
identified that the VEGP management policy and stated practice
,
required preparations for a power reduction, including
8
informing the load dispatcher within the first hour.
' (Discussed in section 2.1.1.3 of Inspection Report 50-424/90-
19; 50-425/90-19)
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with preplanned system outages which were required for i
other preventive or corrective maintenance or testing. i
inspection identified that few of the snubber
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The
modifications were done jointly with pre-planned system j
,
i outages. (Discussed in Section 2.1.1.4 of Inspection
Report 50-424/90-19; 50-425/90-19)
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- . *=14mhl11tyr vrco j
E== v.nq Diesel-Generater (w)
,
.ncorrectly counted the number of starts and failurgot
1 t DGs and incorrectly represented the EDG re ability i
in a on II presentation on April 9, 199 Although t
I the presen ion was not 'ntended to repr sent a specific ,
number of su ssful valid test s specified in l
,
Regulatory Guide ( 1.108 and T . 8.1.1.2a, but rather
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to describe the EDG ma nan test program and the EDG
reliability status, the was not informed of the i
C asked for it during !
j incorrect information il th
i
the inspection. he confirmat of action (CAL)
response and L nsee Event Report (LER -006 were also ,
incorrect A cause they were based on t EDG start l
inform fon that was compiled for the VEGP pre ation !
I
j in e Region II Office. (Discussed in Section 2. f
g[ s inspection report)
I
This is a Severity M vel IV violation (Supplement VII).
2
l B. Technical Specification 6.7.1.a requires that written
j procedures be established or implemented for those activities
' delineated in Appendix A of Regulatory Guide 1.33, Revision 2,
i February 1978.
l Contrary to the above, two examples were identified in which
- the licensee failed to establish or implement the procedures I
- for these required activities as follows: (50-424/90-ac'M? :
50-425/90-asu-49) 19- G
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19 - 6
! 1. Administrative Procedure 00150-C, " Deficiency Control,"
i- states that a deficiency card must be written if the
i deficiency involves safety-related components which are
to be dispositioned "use-as-is/ repair," or other
conditions involving safety-related components which
- require engineering support or other technical assistance
- to determine if the component is deficient.
d
on August 17, 1990, the NRC identified that a deficiency
card was not written on re'idual heat removal (RHR) pump
'
f1B (a safety-related component) to document the pump's
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' degraded conditions which were dispositioned "use-as-is".
(Discussed in Section 2.2 of this inspection report)
i 2. Administrative Procedure 00100-C, " Quality Assurance
- Records Administration," Paragraph 4.1.1.8, specifies
- that quality assurance (QA) records will exh! bit
- necessary and appropriate signatures or initials and
dates.
[
.
- On August 17, 1990, the NRC identified that the Unit
i Superintendent incorrectly initialed, dated, and signed
i a QA record which voided Temporary Change Procedure (TCP)
1802-C-7-90-1 to Abnormal Operating Procedure 18028-C,
" Loss of Instrument Air," with the date of June 12, 1990,
i in lieu of the actual date (June 15, 1990) on which the
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document was signed. (Discussed in Section Jdf of this
i inspection report) g.1b
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This is a Severity Level IV violation (Supplement I). ;
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- C= re. ::, w=n= :. cra.r4 --cI, corr.cu= -
Action," requires measures to be established to ensure tha [
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onditions adverse to quality are promptly identified f d
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c rected. In the case of significant conditions adve Ne to
! qua , the measures are required to ensure that theguse of
i the co tion is determined and corrective action Jd taken to
i preclude tition. /
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ve, two examples were identified in which
Contrary to th
the licensee fa d to determine and adequate
- corrective actions preclude repetitl'o/aplement
n as follows: (50-
l 424/90 .ans- et) / !
i 14 - 14 /
j 1. On August 17,1900, theWC4etermined that the licensee
"
did not identify the foitat and normal use of the 14:0
. status sheet as one oJA.he causes of the event described
in Licensee Event Report (LER) '90,-004, " Failure To comply
j
- With Technical Specification 3.0N< occurs on Entry Into
,
Mode 6"; therefore, corrective action was not taken to
preclude repet'ition of the failure to review Ico-required
actions orAremarks which may be on the back side of the
i LCo status sheet. (Discussed in Section '2.4 of this ,
inspect' ion report) i
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1- 2.
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(chnical Specifications 4.8.1.1.3 and 6.8.2 require hat
,
all valid or non-valid EDG failures be reported to th
NRC in a special report within 30 days. In addition,
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. Operations Procedure 55038-C, " Diesel Start Log," Section
'
. 0, requires that all EDG failures shall be re or(ed to
t RC in a special report.
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On Augu 17, 1990, the NRC ideptified that the
j corrective a ions taken in response 4o a previous notice
'
of violation e inadequate./ Inspection Report 50-
.
424/s7-57 (dated aber Sj A987) previously identified
l a violation of Tech ' al Specification 4.8.1.1.3, in
! that, all EDG failuresmo not reported to the NRC in a
- special report. During a re w of the start records for
i EDG f1B duringA:he period of h 21 through June 14,
i 1990, the NBC' identified that EDG lures had occurred
l which were'not submitted to the NRC in special report.
- In a difion, the NRC identified that Opera ns Procedure
.l 5 8-C provided inadequate guidance to i tify and
- classify EDG failures. (Discussed in Section 2. this
j inspection report)
This is a Severity I4 vel IV violation (Supplement I).
! Pursuant to the provisions of 10 CFR 2.201, Georgia Power Company
is hereby required to submit a written statement or explanation to
Nuclear Regulatory Commission, ATTN: Document Control
,
i the U.S.
Desk, Washington, DC 20555, with a copy to the Regional
Administrator, Region II, and, if applicable, a copy to the NRC
Resident Inspector within 30 days of the date of the letter i
transmitting this Notice Of Viel: tic . (;5tia) . This reply should
be clearly marked as a " Reply to a Notice of Violation" and should
include for each violation: (1) the reason for the violation, or,
if contested, the basis for disputing the violation, (2) the
corrective steps that have been taken and the results achieved, (3)
the corrective steps that will be taken to avoid further
violations, and (4) the date when full compliance will be achieved.
If an adequate reply is not received within the time specified in
this Notice, an order may be issued to show cause why the license
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should not be modified, suspended, or revoked, or why such other
action as may be proper should not be taken. Where good cause is
shown, consideration will be given to extending the response time.
,
FOR THE NUCLEAR REGULATORY COMMISSION
l
Stuart D. Ebneter
Regional Administrator
Region II
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Dated at Atlanta, Georgia
(s r ov\ !
this day of 199p
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R.ePeer
Eid Judu,6 4
Te w ts
Report No.: 50-424/90-N and 50-425/90-N , $u f pleMe aN I
Licensce: Georgia Power company
P.O. Box 1295
Birmingham, AL 35201 .
Docket Nos.: 50-424 and 50-425 License Nos.: NPF-68 and NPF-81
Facility Name: Vogtle Electric Generating Plant, Units 1 and 2
i
Inspection Conducted: August 6-17, 1990
1
Team Members:
Ron Aiello - Resident Inspector, Vogtle
Morris Branch - Senior Resident Inspector, Watts Barr .
'
Robert E. Carroll, Jr. - Project Engineer, DRP, Region II
Larry Garner - Senior Resident Inspector, Robinson
Neal K. Nuneauller - Licensing Examiner, NRR
Larry L. Robinson - Investigator, 01, Region II
Robert D. Starkey - Resident Inspector, Vogtle
Craig T. Tate - Investigator, 01, Region II
Peter A. Taylor - Reactor Inspector, DRS, Region II
McKenzie Thomas - Reactor Inspector, DRS, Region II
' John D. Wilcox, Jr. - Operations Engineer, NRR
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' Team Leader:,. _ _ __. _ _ --
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" Chfis E Va'nDenburgh, SectTon C'hief
Division of Reactor Inspections and Safeguards
! Office of Nuclear Reactor Regulation
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Appeeved by: _ .
- - ::,re e:r r.y.5g,a q
a s . ten m< =~e m. --3 =t a - gg jg i
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TABLE OF CONTENTS
suf Wf
g 90,
INSPECTION SUMMARY........................................ -t"
1.0 INS PECTION OBJ ECTIVES . . . . . . . . . . . . . . . . . . . . . . . . . ..... T'
2.0 ALLEGATION FOLLOWUP.................................. Ar
2.1 Improper Installation of FAVA System............ 9-
2.2 Operability of Residual Heat Removal Pump....... 41-
2.3 Mi.e.d -Ce..teinsent Isc1; tion '!;1v; Ourveillance. 10
2.4 Msde Cheng; "'ith In:perable Source Rang?
3 -Moni te r Ne:l e r ! n t re :n t . . . . . . . . . . . . . . . . . . . . . . 10-
2 .JF Backdating o f Signatures. . . . . . . . . . . . . . . . . . . . . . . . jkP
2.sr Reportability of Previous Engineered Safety
Y Features Actuation System Load Sequencer
Outages......................................... 24'
3.' Reliability cf Esergency Olcsci Cenereters. . . . . . 2-
2.,r Air Quality of Emergency Diesel Generator
6 Starting Air System............................. 34F
2.F b Reportability of Previous System Outages........ 25'
'2..'7 .240 Intimidation of Plant Review Board Members. . . . . . 33-
2 b L kT Personnel Accountability........................ ,3&-
3.0 EXIT INTERVIEWS...................................... )4P
APPENDIX 1 - LIST OF TRANSCRIBED INTERVIEWS. . . . . . . . . . . . . . . JFr
APPENDIX 2 - PERSONS CONTACT 2D. . . . . . . . . . . . . . . . . . . . . . . . . . . . J1r
APPENDIX 3 - LIST OF ACRONYMS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . ,$8
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INSPECTION SUMMARY
Recent activities which have occurred at the Vogtle Electric
Generating Plant (VEGP) have raised concerns within the Nuclear
Regulatory Commission (NRC) as to the ability and the deterinination
of the licensee to operate the facility in a safe and conservative
manner. To address this concern, the NRC performed a special team
inspection to deter 1mine if the licensee operates the facility in
accordance with approved procedures and within the requirements and ,
intent of the facility's operating license. In addition to the !
occurrence of specific events, NRC concerns regarding the safe
operation of the facility were heightened with the receipt of
several allegations relating to operational activities at VEGP.
The aggregation of the facts and circumstances associated with the
operational events and the allegations was viewed as a possible
indicator of a non-conservative attitude on the part of the
facility's operating staff which warranted the immediate initiation I
of special inspection activities.
Specifically, the inspection objectives were to:
1) Assess the operational philosophy, policy, procedures and I
practices of the f acility's operating staff and management I
'
regarding operational safety.
2) Determine the technical validity and safety significance of
- d cf the allegations and their impact on the safe and {
conservative operation of the facility.
These inspection objectives were accomplished by the use of two
inspection teams--an operations followup team and an allegations
followup team. The offorts of these two inspection teams were
closely coordinated; however, they independently pursued the
objectives outlined above.
The operations followup team monitored control room activities on
a 24-hour basis in order to: (1) evaluate the operational
philosophy, policies, procedures, and practices of the operating
. staff and management and (2) determine if the plant was being
i operated in a safe and conservative manner in accordance with the
l facilities' operating license.
!
- The allegations followup team verified the technical validity and
safety significance of each ef the allegations. In addition, with k
the assistance of the OI staff, this team interviewed * members of
4 the plant staff in order to determine (1) their personal
j involvement and knowledge of the specific allegations and (2) their
- practice and understanding of the station operational policies.
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! These-interviews were transcribed. Although an OI investigator was l
l assigned to the inspection team to assist during the transcribed !
1 interviews, this inspection was not an investigation into th g
! intent of the alleaed violations. Nu muesrep.a5 **t M *M }
,
w (:iewen. e<mo not iunst.
The inspection substantiated the occurrence of the specific events
q
described in the allegations. These events resulted i t
i
examples o v, lations of regulatory requirements (50-424/90- D l
'
50-425/90- )2' "" G/^; .. ;^ ; and two of the events were .
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! previously identified as non-cited violations (50-424/90-10-03 and d
50-425/90-01-01). ::: : : , the ine;rrtier did net rubettntirt
-th:t th: : ::t: :' vielstien vere-perfe n f rith the full-
l
j L,wledge of 'J::Or ::n:; ::nt. Sie cerclerier See herM rper :
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' ;vice Of the lic:::ee's recorde ^^d the Svern testisery ef the
j pe;ple inv;17;d in th: ev::t;.
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inspection also identified that on several oc
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) naccurate
i respons agers and supervisors verbally su
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information to t e ' tion team durin spection. Although l
the inspection team was a out the accuracy of the i
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J information provided an did n a basis to conclude or l
i suspect th examples were the result o ss disregard ,
'
atory requirements or individual wrongdoing. 1
I
Ioom
- - --- m.' ' b observations and conclusions of the inspection tem #g::o )
are detailed in Inspection Report
50-424/90-19; 50-425/90-1C
/
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addition, the bases for these previous conclusions are summarizedIn ,)#-
4
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below.
3 Doerational Policies and Practices
i NRC Inspection Report 50-424/90-19; 50-425/90-19 identified several
- examples in which the licensee's operational policies and practices
'
had the potential to adversely affect the operation of the
i facility. llegation followup team's review of the allegations
- identifiedn additional examples in which the licensee's l
l
operational policies and practices had the potential to adversely
affect the safe operation of the facility 1 "^r err;1:- {
I 1) The licensee's method of conducting Plant Review Board (PRB)
,
meetings had the potential for adversely affecting open
i discussions among the PRB members. This concern was based on
i an example in which a PRB voting member felt intimidated and
4
feared retribution during a PRB meeting because of the
presence of the general manager and the absence of dissenting
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opinions in the PRB meeting minutes. Continued licensee
action is necessary to ensure that PRB members freely and
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openly express their technical opinions and safety concerns.
, (Section.2AC)
i Z7
i 2) The licensee's practice of signing and dating quality
i assurance records was controlled by administrative procedures;
j however, there was a confirmed exasple in which a signature
j was backdated to reflect the actual date of performance. The '
} backdating of TCP 1802-C-7-90-1 was verified and was l
1 identified as Violation 50-424/90- ' ~6; 50-4 25/90-aus-et .
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(Section 24) i
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l 3) The licensee' practice of not initiating a deficiency card
(DC) during troubleshooting activities involving the
questioned operability of the residual heat removal (RHR) pump
prevented a documented engineering evaluation for either the
nuclear service cooling water (NSCW) outlet leak or the
excessive vibration on the RHR motor. The fal' lure to
, implesent this administrative procedure was identified as .4
1 Violation 50-4 2 4/90 .xas-@2. (Section 2.2)
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.. :the ef 59*= 4 = 4 a0 ==d eaaWal l i a; en,a 4 == af
, completed surveillance procedures was not controlled y
- inistrative procedures. Based on the confusio hich
i resu d in the missed curveillance of the tainment
j' isolatio alves and a review of this methodo additional
3 atter. tion acessary to ensure that thg procedures are
2
appropriately c ntrolled and used. (Sect' ion 2.3)
- ,9) The licensee's math to denti tive and informational
limiting condition for oper .ns (Iros) on LCO status sheets
allowed continuation o he ~I40 required ac.tions on the
reverse side of the rm. This me , in conjunction with
'
the operator's c reed practice of re wing only the front
side of the status sheets, was one of oot causes for
l a non-ci violation (50-424/90-10-03) conc ng a mode
l cha ich occurred with inoperable source ra uclear
- i ruments. The failure to identify this additiona oot
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v.u.. ... la.ni.iii.4 es Vicletie.. 50 4 ?/00 :: ^3. (!::t _ _
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fW The licensee's method of appraising the performance of the
licensed operators resulted in a potential disincentive for
identifying items which may result in LERs or violations,
j (Section 2 44) l
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Accuraev of Information I
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The inspection concluded that during the inspection inaccurate '
' information was received on several occasions, from responsible
managers and operators on topp:s well within the scope of * a ir
specific responsibility. In 4Manstances the initial infor Cisn (
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supplied was clearly incorrect or inadequately researchef th t :
l inspection team concluded that in each of these example:
licensee officials provided inaccurate, unsworn, oral stat cent s
1
concerning information which concerned topics well within ts.24r :
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responsibilities,
i ho inaccurate information was
- the 4ir;t th::: cases, the { l
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significant to the inspection process. Specifically, (1) if the
i
' containment isolation valves received an automatic closure signalthe v
' if the snubber modifications had been performed in conjunction with
i other preplanned preventive and corrective maintenance, then the ;
voluntary entries into LCO 3.7.8 would not have been required, end- I
.
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p) ii the-WRC-was.. accurately informed .cf.-the-aumber of 15 p ehich 51:::
1 and i.ilorse ;' - th: Ere:gency Diesel Cenerator-No.
uwwuu.a dosinii ts d10 h:: ting, ther additiert! tecting rey hr : j
,.... . .,,. is .4- pries to - th: rele::: .. .... ....... _..... .. ::tden l
1etten The inspection team concluded that the failure to provide !
accurate information was a violation of the requirements of 10 CFR
50.9 concerning accuracy and completeness of information. The
inspection identified Violation 50-424/90- ; 50-425/90-Jsw-99 in
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this area and ncted the following examples:
containment Isolation valves: During a Unit 1 surveillance
,
! 1)
procedure, the unit shif t supervisor (USS) stated, and the
,
operations manager later confirmed, that the containment
isolation valves for the hydrogen monitor system were allowed
to be opened without entering the 140 action requirements for
.
i TS 3.6.3 because the talves received an automatic isolation
i signal. The inspection identified that these containment
i isolation valves were remotely-operated, manual valves without
I auta.tatic isolation signals. (Discussed in Section 2.2.1.1 of '
Inspect Dn Report 50-424/90-19; 50-425/90-19)
2) Snubber Reduction: The operations manager stated that, after
Unit 1 refueling outage IR2, the modifications to the snubbers
were done in conjunction with preplanned system outages which i
were required for other preventive or corrective maintenance
or testing. The inspection identified that few of the snubber
i modifications were done jointly with pre-planned system
' outages. (Discussed in Section 2.1.1.4 of Inspection Report l
50-424/90-19; 50-425/90-19) j
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Emeraenev Diesel cenerator Reliability: The licensee's met
researching information for Region II prese ion
conc {
ng the reliability of the emergency diesel , erators !
(EDGs) v nadequate in that there was a 1 of specific l
. guidance conc ng the EDG information d red coupled with I
inadequate resear the EDG starti story. This method l
resulted in providing omplete , therefore, inaccurate
info mation to the NRC. inn lon, the licensee's response i
to the NRC's confi nation ac letter (CAL) was based on
,
this same inadequate earch. In tion, the subsequent i
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Licensee ' Event rt (LER)90-006 was so inadequately !
researched. a result of this method of inv ation, the i
NRC was r informed of the correct operability a until j
this pection. (Discussed in section 2.7 of this inspe n
ort) !
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34t Personnel Accountability: Theoperationsmanagerstatedthatl !
the shift superintendents (sss) reported directly to the '
operations manager and that he personally prepared their i
performance appraisals. The inspection identified that the :
SSs reported to the unit superintendent (US), and that the US I
personally prepared the performance appraisals of the SSs. !
(Discussed in Section 3 A 1 of this inspection report) {
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4pf ts 3. 0. 3 Actione: The unit superintendent indicated that l !
there were no operations Department actions which were
anticipated or required within the first three hours of i
i
entering the action statement of TS 3.0.3. The inspection !
identified that the VEGP management policy and stated practice !
required preparations for a power reduction, including
i informing the load dispatcher within the first hour.
i
j (Discussed in Section 2.1.1.3 of Inspectica Report 50-424/90- i
' its 50-425/90-19) ;
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- In summary, the inspection identified these violations and two\ r
' inspector followup items. The violations involved: (1) a violation i
of 10 CFR 50.9 in that responsible licensee officials provided
inaccurate information to the NRC during the inspectionf4(2) a ,
violation of TS 6.7.1.a in that, two examples were identified of k
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the licensee failing to }mplement actions in accordance with
l administrative procedures /, M _f') : vi:1;ti... . M 0.7 n, .
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W '. 2, 0: iter!:: "Y!, in th:t, tt:0 ::: ;1 : ::: id:nti f'<ed-of !
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The inspection also identified two inspector followup items ,
involving: (I) an unreviewed safety question concerning the use of ;
the alternate radwaste building, and (2) the lack of operator
guidance concerning the applicable limiting conditions of operation
during engineered safety features actuation system sequencer ;
outages.
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INSPECTION DETAILS l
1.0 INSPECTION OIL 7ECTIVES
Recent activities which have occurred at the Vogtle Electric
Generating Plant (VEGP) have raised concerns within the Nuclear
Regulatory Commission (NRC) as to the ability and the determination
of the licensee to operate the facility in a safe and conservative
manner. To address this concern, the NRC performed a special team
inspection to determine if the licensee operates the facility in
accordance with approvad procedures and within the requirements and
intent of the facility's operating license. In addition to the
occurrence of specific events, NRC concerns regarding the safe
operation of the facility were heightened with the receipt of I
several allegations relating to operational activities at VEGP. l
The aggregation of the facts and circumstances associated with the
operational events and the allegations was viewed as a possible
indicator of a non-conservative attitude on the part of the i
facility's operating staff which warranted the immediate initiation '
of special inspection activities.
Because a non-conservative attitude or operating philosophy may j
represent a hazard to the health and safety of the public, a l
special inspection team comprising staff from the Region II Office l
and the Office of Nuclear Reactor Regulation (NRR), assisted by '
staff from the Office of Investigations (OI), was formed to
determine the individual validity and collective impact of these
allegations on the safe operation of the facility. The purpose of l
the inspection was to determine if the licensee operates the j
facility in a conservative and safe manner in accordance with
approved procedures, and the intent and requirements of the
facility's operating license. Specifically, the inspection
objectives were to:
1) kssess the operational philosophy, policy, procedures, and l
!
practices of the facility's operating staff and managemenc l
regarding operational safety. )
, 2) Determine the technical validity and safety significance of l
each of the allegations and their impact on the safe and '
, conservative operation of the facility.
l These inspection objectives were accomplished by the use of two
inspection teams--an operations followup team and an allegations
- followup team. The efforts of these two inspection teams were
closely coordinated; however, they independently pursued the
obj a::tives outlined above.
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j Theoperationsfollowupteammonitoredcontrolroomactivitieson(
a 24-hour basis in order to: (1) evaluate the operational 8 !
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philosophy, policies, procedures, and practices of the operating 3
3 ' staff . and management and- (2) determine if the plant was being' .
!
operated in a safe and conservative manner in accordance with the g !
facility's operating license. 3 !
C ,
The specific inspection activities of the operations team was :
described in Inspection Report 50-424/90-19 and 50-425/90-19g e ,.
efforts and conclusions of the allege8 _ti_ ops followup teams are i
described in this inspection report. " In addition, this report } l
identifies several violations 2nd $2;;..;i:1 ;;;%..;;;;; in the l
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licensee's :;;reti;nci pr!!:ler, prr;r-- , and procedures. 9he- ;
gecificdetails==d h:;i; fe; th; ine;::ti:r trer's r---=ea= are
detailed in the sections that follow and in the Inspection Summary.
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2.0 ALLEGATION FOLIDWUP
The inspection team reviewed several allegations for their
[
technical validity and interviewed licensed and non-licensed !
personnel to determine their personal knowledge and experience !
regarding these issues. This portion of the inspection was j
performed to determine the validity and significance of the .
allegations. 5:::r:: the elle;stierr errerted *Mt li--- ed '
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- :: 5:d vieleted the Techair:1 Sp^cificatiene (??) vith the !
h.:rl:d;: f lieerrer rare;r rrt, *he inepretien t:22 revier:d th: '
cirrrrrtencer e-d retienele fer i=dividerl retic- . '
The inspection of the allegations included technical reviews of the
licensee's records, logs, and interviews of the personnel involved
in the alleged violations. Although a transcribed record was not
required for every discussion with the licensee's staff, the
inspection team conducted sworn, transcribed interviews with
selected individuals in order to document (1) the individual's
personal knowledge and involvement in the alleged violations and
(2) the circumstances and rationale for their individual actions.
Although an of investigator was assigned to the inspection team to
assist during the transcribed interviews, this inspection was not
an investigation
ewr cos into .the
ar 7w Anap Aur.sers 5 m intent
Amp.rc ofghe h alleaed vi.olations. TwaM
p c. m n Cnc ,ys s,.
The interviews were transcribed after the technical evaluations of
the allegations in order to permit a focused interview and to
minimize the length and scope of the transcribed proceedings.
,
The
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transcribed interviews are listed in Appendir 1 in the order they j 4 p
were conducted. The sworn testimony was th? 5;;;6on wnica the
inspection team reached its conclusion on each of the allegations.
These conclusions are prcsented in the material that follows
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(Sections 2.1 through W ). ' '
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- 2.1 .Imoroner Installation of FAVA System
i
An allegation indicated that VEGP installed and operated a radwaste
nicrofiltration system, known as the FAVA system,
j without !
performing an adequate engineering and safety evaluation (i.e.,10
!
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CFR 50.59). Furthermore, the material configuration, fabrication i
and quality of the system did not meet the guidance of Regulatory
.
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Guide (RG) 1.143 and the requirements of the American Society of
.
Mechanical Engineer's (ASME) Code.
1
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The FAVA system was temporarily installed for removing Niobium-95.
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The system was later determined to be better suited for as-low-as- ,
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i reasonably-achievable considerations during refueling outage IR2, i
particularly for removing Cobalt-59 and Cobalt-60. VEGP planned to
i replace this temporary modification with a permanent, high-
j; quality, steel system in the future; however, the health and safety l
of the public may be jeopardized if a break in the system i
- (resulting in a radioactive release to an unrestricted area)
occurred in the interim. i
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j Discussion i
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- In February 1988, the VEGP experienced difficulty in removing [
colloidal Niobium-95 following a reactor shutdown for maintenance
work. i
- FAVA Control Systems (FAVA) was hired to help rectify this
problem. FAVA was selected because of its experience in filtration
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and domineralization. The situation was corrected by installing !
i a 0.35-micron filter system downstream of the existing vendor-
supplied pre-filters. t
i generated as the 0.35-micron filters
However, a large volume of radwaste was I
i rapidly exhibited high
- differential pressure and were required to be changed frequently.
!
The need to change filters frequently also resulted in additional
!
radiation exposure to Radwaste Department personnel.
j Upon evaluation of the performance of the 0.35 micron filter
system, the Radwaste Department felt that the best approach to the
problem was a back-flush, pre-coat filter system. However, no
j
operational data was available for a system of this type in this
specific application. FAVA supplied a proprietan Ultra Filtration
3
System (Model No. SFD/E) for testing purposes in order to evaluate
- whether
problem. or not this was a viable and economic solution to the
i The FAVA system was installed before the Unit I refueling
j
outage and was operated under Test Procedure T-OPER-8801. The test
,
system kept liquid effluent releases well below TS limits. on the
basis of an evaluation of test results by the Radwaste, Chemistry,
and Engineering Departments, a general work order was initiated to
l purchase a permanent system.
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In the early part of 1989, a Quality Assurance (QA) Department :
audit identified a significant audit finding involving a
programmatic breakdown in the procurement of the FAVA system and !
i the failure to meet commitments of the Final Safety Analysis Report
!
(FSAR).- Because of that finding, the FAVA system was removed from
service. In late 1989, the licensee sought to reinstall the FAVA ,
i system under a temporary modification because colloidal Cobalt-59
i and Cobalt-60 had to be removed. The Plant Review Board (PRB)
,
reviewed this temporary modification and several members expressed
] strong objections to it based on the previous QA audit finding.
-
>
i Subsequently, a request for engineering assistance (REA) was :
i submitted and a 10 CFR ' 50.59 safety evaluation was performed in
i late 1980. This safety evaluation did not properly address the
i
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guidance of Regulatory Guide (RG) 1.143 regarding the use of
polyvinyl chloride (PVC) piping.' Therefore, another safety
- evaluation was p rformed in February 1990 to address this issue--- l
j particularly with respect to radiation degradation.
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The February 1990 safety evaluation specifically stated that the 1
l
FAVA system did not conform to the criteria of RG 1.143. This
! '
deviation was found to be acceptable for the following reasons:
'
1) The design of the FAVA system had been previously evaluated
! and found to be adequate in the response to REA VG-9057 dated
l November 28, 1989 (log SG-8592).
l 2) The location of the FAVA microfiltration system inside a
i
shielded, watertight vault provided adequate assurance that
- any system failures will be contained and would not create the
l potential for offsite releases of, radioactivity.
.
l 3) The presence of PVC pipe in the FAVA system, although
l- prohibited by RG 1.143, was acceptable because the radiation
i
exposure to the plastic was within acceptable limits for up to
i 6 months based on the following:
!
a) The amount of PVC piping used was not extensive and was
j contained on the FAVA filter skid.
1
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b) There were no reported leaks or malfunctions during the
' approximately 6 months that the FAVA system filter was
previously in use,
d
c) Since the FAVA system filter skid was located within the
demineralizar vault, it would be protected from being
damaged.
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I d) On the basis of the assumed' length of time that the PVC .
! piping would be used in a radioactive environment and the
- activity levels of the effluent at this stage in the
! liquid radwaste process, the integrated dose to the PVC 'I
- piping would be well below the radiation damage threshold !
! for PVC pipe as reported in Electric Power Research '
i
Institute (EPRI) Report NP-2129, dated November 1981
! (i.e., 6.5 rad over a 6 month period versus the radiation
j: damage threshold of 5.0 x los rad) .
i e) The PVC pipe would not be subjected to excessive pressure !
i
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conditions since the maximue. available inlet pressure to i
!
the filter was so to 100 pounds per square inch gauge !
(psig) which is well below the maximum allowable working
, pressure of 120 psig for the PVC pipe. j
f) The system could be operated at design-basis conditions !
for 182 days before it would exceed the radiation damage
i
threshold. However, under conditions currently existing
.
at the plant, the expected dose to the PVC piping will
j less than 0.1 percent of the design basis.
i Although the testamony of one of the PRB members indicated that the
,
temperature effects on the use of PVC in the FAVA System were not
i
adequately evaluated before the system was installed, the testimony
! of the corporate system engineer indicated that this was considered
i
prior to installation, although not specifically documented in the
- safety evaluation.
1
1
The VEGP general manager subsequently consulted the NRC resident
! inspector to seek an NRC position with regard to placing this
1- system - back in service. This was supplemented by information
{
' documenting reasons why it should not be placed in service. This
package was forwarded to Region II and the office of Nuclear
Reactor Regulation (NRR) for review. In March 1990, following
Region II and NRR concurrence via a telephone conference, the
licensee placed the FAVA system in service with the following NRC
! stipulations:
I
j 1) Procedures for operating the FAVA system required an operator
,
j
to be in attendance for the entire length of time the systra -
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would be in operation.
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2) All hoses going to and coming from the FAVA syst en required
! verification that they met the requirements of RG 1.143.
1
- 3) The cover over the FAVA system wa- required to be securely
- fastened when the system was in operation to ensure that if a
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i spraying leak developed, it would be contained in the concrete
l vault.
i-
4) The design of the . walls of the alternate radwaste building !
!
(ARB) was required to be evaluated to determine whether or not
i a design modification should be made to reduce the potential ?
j of wall leakage in the event that a hose leak developed and
j sprayed its contents on the walls.
,
i In June 1990, in response to item 4 (above), the licensee revised
Part G of the safety evaluation for the FAVA system. Part G of the
i safety evaluation addressed the effect that operation of the FAVA 1
! system would have on the probability of occurrence or consequences ,
{ of accidents described in the FSAR. Although there was no l
4
comparable accident analysis in the FSAR that addressed the ARB
accidents or the consequences of accidents in the ARB, the FSAR
I accident analyses (Chapters 15.7.2 and 15.7.3) did describe worst-
- case releases of the contents of the recycle holdup tank (HUT) .
l'
The first bounding analysis in Chapter 15.7.2 addressed the release
of the entire gaseous radioactive contents of the HUT to the
i'
environment at ground level and the second bounding analysis {
addressed the release of the entire liquid contents of the HUT-
i through an assumed crack 2n the ARS floor directly into the ground !
- . water supply. In both cases, the 10 CFR Part 100 and 10 CFR Part 1
'
20 limits were not exceeded. These criteria were consistent with
'
j criteria provided in NRC Circular 80-18, "10 CFR 50.59 Safety l
Evaluations for Changes to Radioactive Waste Treatment System." '
- However, neither of these analyses addressed the potential for wall
- spray down and leakage. through the ARB walls and the subsequent
t release path to the environment. Therefore, the licensee revised
the safety evaluation in June 1990 to address the consequences of
i
a hose break on the FAVA system which would result in wall spray
l
down and potential leakage to the environment.
,
l The inspection team's review of the revised Part G of the safety
i evaluation identified several erroneous assumptions with respect to
the release path and the dilution volumes that could be used in the
,
analysis of a hose break and resultant wall spray down. However,
the inspection team also found that the design of the FAVA system
- (i.e., the use of a system cover) would prevent wall spray down and
that the only potential source for wall spray down and subsequent
leakage was from a hose break in another radwaste system in the
- ARB. Therefore, the inspection team concluded that the FAVA system
safety evaluation dated June 1990, adequately addressed the
.
temporary modification for the installation of the FAVA system;
j however, the inspection team's review identified an unreviewed
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safety question concerning the release paths and consequences of a !
failure of the other radwaste systems in the ARB.
In' addition, the team noted that in Supplements 3 and 4 of the
Safety Evaluation Report (SER), the NRC staff reviewed and accepted ,
,
the design of the ARB and specifically addressed the consequences
of a hose break on a radwaste system in the ARB. However, the SER
supplements addressed the effects of high airborne activities and
,
puddling and did not address the potential for wall spray down and
leakage. The ARB was installed before the plant was licensed;
t
' therefore, the NRC approved the design and use of the ARB in )
Supplements 3 and 4 of the SER. Thus, there was no requirement to !
perform another evaluation of the potential effects of hose brcaks
on systems other than the system being installed by the temporary
modification (i.e., the FAVA system).
1
Because the design of the
l
FAVA system effectively prevented a wall spray down, this was not ;
' a concern that was required to be addressed by the FAVA system '
safety evaluation. Nevertheless, now that it has been identified,
l
l the consequences of a hose break and wall spray down in the other
4
ARB radwaste systems must be resolved. Therefore, this issue will
be followed as an inspector followup item pending further review
and evaluation and is identified as:
- ' 19 -14 19 - N
IFI 50-424/90.x*-07 and 50-4 2 5/ 9 0-xw-02", 'Dotential Unreviewed
Safety Question Regarding Spray Down of the Alternate Radwaste
Building." .
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- Conclusion l
Although the FAVA system was originally installed without an
3
adequate safety evaluation and did not meet the regulatory l
guidance, the inspection team concluded that the subsequent safety i
evaluations were acceptable for the system's use. Serefert, th;
1
' inerrtien tem cen:1 d:d that th; ellgeti;n iter ne* M 1y ) l
r Arte el.i d. (
As a result of QA Department's significant audit finding in early
1989 involving a breakdown in procurement and failure to meet FSAR
- commitments, the system was removed from service. Subsequently, ;
the FAVA system was returned to service following two safety j
,
evaluations which adequately addressed the use of PVC piping with I
respect to radiation degradation and pipe rupture. Therefore,
these safety evaluations justified the use of the FAVA system, even
though the recommendations of RG 1.143 and ASME Code requirements
were not met. Although the safety evaluations did not specifically
address high-temperature effects, the testimony indicated that
these effects had been considered before the system was installed.
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Although the safety evaluation performed in June 1990 at the
, request of the NRC Region II Office did not adequately evaluate the
!
effects of a wall spray down and wall leakage to an unrestricted
area, this evaluation was not required because the FAVA system has
a protective cover and the use of hoses and effects of hose breaks
(i.e., airborne activity and puddling) were addressed in SER
J
Supplements 3 and 4.
I
Regardless of whether the safety evaluation was required to address
the effects of a break in the hoses (which could result in wall
spray down or leakage), the inspection team identified a new
concern involving the use of the ARB because the safety evaluation
inadequately addressed the potential effects of wall spray down
l from any other source in the ARB owing to erroneous assumptions
- concerning the release path and the dilution volumes. This is a
<
potentially unreviewed safety question concerning the use of the
alternate radwaste building.
2.2 Operability of the Residual Heat Removal Pumo
'
An allegation indicated that during Unit i refueling outage IR2
with residual heat removal (RHR) Train A out of service for
maintenance, the Train B RHR pump experienced excessive vibration
and a nuclear service cooling water (NSCW) motor cooler outlet
i
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leak. In addition, TS 3.9.8.1, "RHR and coolant Circulation," was
allegedly violated because the operations Department chose not to
, declare RHR pump 15 inoperable in an effort to mitigate the impact
on the critical work path.
Discussion
TS 3.9.8.1 requires at least one RHR train to be operable and in
operation during Mode 6 (refueling) when the water level above the ,
top of the reactor vessel flange is 23 feet or more. Otherwise, '
Suspeed all operations involving an increase in the l
reactor decay heat load or a reduction in boron i
,
concentration of the reactor coolant system (RCS) and j
!
Immediately initiate corrective action to return the '
I
required RHR train to operable and operating status as
soon as possible and close all containment penetrations
'
providing direct access from the containment atmosphere
to the outside atmosphere within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />.
The inspection team verified that during Unit I refueling outage
IR2 with higher than normal vibration measurements on the RHR pump <
4
1B and a leak on the NSCC outlet of the Rh motor cooler,
Department did
'
operations personnel not declare the pump ;
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i
i inoperable. This determination was made after consulting with the
on-shift duty engineer from the Engineering Department and was !
, based on the determination that the pump would fulfill its intended '
j
!,
safety function in Mode 6. Specifically, the RHR pump was capable
of removing decay heat from the partially defueled reactor core.
j The testimony of the individuals involved indicated that this .
. operability determination was based on the fact that the vibration
- readings taken at the inservice test (IST) surveillance points did
not reach the IST Alert levels and were therefore acceptable for
- continued service. Although the high vibration readings on the top
.
end of the RHR pump were later determined by the vendor
-
(Westinghouse) to be excessive, at the time of the operability i
- evaluation, the licensee accepted these values, regardless of their
f
magnitude, because the readings at IST test points were below the
I Alert levels. The testimony also indicated that, even with a leak l
l on the NSCW outlet of the RHR motor cooler, the motor was receiving '
j full cooling water flow and cooling would not have been immediately
i compromised following a complete NSCW discharge pipe break.
l Furthermore, the. testimony indicated that the operations Department
j had : implemented compensatory actions to monitor the vibration
- levels and NSCW 1eakage and ensure the continued operability of the
l pump by stationing an operator at the RHR pump to monitor the
- vibration levels and notify the control room if the vibration
,
levels increased, thus allowing the control room to implement the
actions of the limiting condition for operations (140).
The inspection team also noted that in event of a catastrophic
!
failure of the RHR pump, all the required actions of TS 3.9.3.I i
I
(i.e., closing all containment penetrations)
'
could have been
$
completed within the required 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> time period of the 140 because
-
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the Ito for TS 3.9.4, " Containment Building penetrations," was in
effect during this time period. This LCO was implemented due to
,
the movement of irradiated fuel from the core to the spent fuel
j
4
pool. The 140 required that,
The equipment door be closed and held in place by at
least four bolts; at least one door in each airlock be
closed; and each penetration providing direct access from
1,
the containment atmosphere to the outside atmosphere
i shall be either closed by an isolation valve, blind
.
flange, or manual valve, or be capable of being closed by '
an operable automatic containment ventilation isolation
j valve.
4
As a result of the implementation of TS 3.9.4, the only remaining
act' .n for the LCO of 73 3.9.8.1 would have been to close the
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containment purge valve which receives an automatic closure signal *
'
and could have been isolated within the Iro action times. !
4 During the course of this review, the inspection team found that
the licensee failed to initiate a deficiency card for either the !
i NSCW 1eak or the excessive vibration as required by operations !
4 Procedure 00150-C, " Deficiency Control." This procedure requires i
'
i that a deficiency card be written if the deficiency involves
- safety-related components which are to be dispositioned "use-as- i
i is/ repair," or other conditions involving safety-related components ,
which require engineering suppolt or other technical assistance to i
determine if the component is deficient. Failure to establish,
,
implement, and maintain adequate operating procedures represents a ,
1 violation of TS 6.7.1.a. This item is identified as:
R-G 6 I
.' VIO 50-424/90_xx=Gt,i..a ;; = /;0 m ;i, " Failure To Establish or
l Implement Procedures for Required Activities."
h conclusion ,
!
!
The inspection team c luded tht t.5e 11-v. tis, n; n;t frily '
i c ertentistrf L;;.;;.3 e operations Department had an adequate i
! engineering basis for accepting the operability of the RHR pump in
j spite of the pump's deficiencies. In addition, the team concluded i
j that declaring the pump inoperable would not have impacted the
! critical work path: the 140 actions would not have been restrictive
'
because containment (excluding ventilation) had been isolated as
,
, required by TS 3.9.4. The LCO actions would not have prev . ,ad the
- continuation of refueling activities because the actions to close !
- all containment penetrations providing direct access from the !
containment atmosphere to the outside atmosphere would only have 1
required closing the containment purge valve which has an automatic
closure signal.
l In addition, the inspection team identified that the licensee
- violated the station's administrative procedures by failing to
,
initiate a deficiency card for either the NSCW outlet leak or the
- excessive vibration on the RNR motor as required by Operations
'
t
Procedure 00150-C.
,
-?' "!:rrf cert fr ent I:02: tier V:1:: Ourec ill;; ca -
l An allegatio icated that a unit shift isor (USS)
concealed the correc time for a T o prevent a forced
i- shutdown of the unit and to '
CFR 50.72 notification to
- the NRC. Furthermore, c ent . ion valves (CIVs) which
'
were missed durin rveillance test sho va been declared
!- inoperabl e immediata actions of the TS LCO s ave been
1 i at the time the missed surveillance was identifie .
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ddition, delaying the initiation of the deficiency card (DC) unt 1 :
i.
t surveillance had been re-perfonned allowed the licensee o i
av (d the immediate actions of the LCO and allowed the un to i
) rema'in in operation and avoid the immediate NRC notificatio .
Discus on
! The inspe tion team reviewed the documentation of a missed
j
surveillanc on the containment isolation valves escribed in
a Licensee Eve Report (LER)90-001 for which a non- ted violation ;
(50-425/90-01- 1) was issued. The LER identified hat during the
i review of mont y Surveillance Procedure 1447 -2, " Containment >
!
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Integrity Veriff tion-Valves outside Contain nt," the licensee :
discovered that 3 CIVs had been overlook and had not been
i tested. In additi ,
the valves had not b en tested during the
<
previous two month 1 s surveillances. Up identification, the
j operating shift re-performed the com ete surveillance and
initiated an investigat n which resulte in a deficiency card (DC)
!
for the previously misse surveillance .
i
i
root cause of the violation was
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The LER indicated that t
personnel error in reviewing t e co lated surveillance task sheet. i
In addition, the computer softv which generated the surveillance
l- task sheets (STS) has been a ified so that it is no longer
!
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possible to inadvertently t n incomplete listing of the
equipment. Even if an error imil to the one which resulted in
.
only two valves being shown n the S were to recur, it could only
result in either all or n e of the e ipment being listed,
i The inspection team v rified that S 3.6.1.1, " Containment
! Integrity," 140 actio statement requi d restoring containment
l integrity within 1 ur or commencing unit shutdown to hot
-
standby within the n t 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />. A shutdo required by Technical .
Specifications wou d have required that th NRC be immediately
s
notified in accor ance with 10 CFR 50.72.
!
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The inspection aan found that the CIV surveillance requirement of
i TS 4. 6.1.1. a ad been completed and approved. The surveillance
, procedure r ired verification every 31 days that al penetrations
i
not capabl4 of being closed by operable containee t automatic
i isolation / valves and required to be closed durin accident
conditi ns be closed by valves, blind flanges, or d etivated
)
'
autom ic valves secured in their normal positions. Du ing the
next shift, the oncoming shift supervisor noted th the
su elllance procedure was only partially performed and that 9 of
'
t CIVs on the surveillance procedure had been marked as ot
pplicable" and had not been performed.
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!'
TS\.0.2.a
witft4n therequires
specifiedthattimeeach
intervalsurveillance requirement be perforud
exten) with a maximum allowa ee
ion not to exceed 25 percent of the surveillance inte
In aditition, Ts 4.0.3 requires that al.
failure to perf
survell
constitut
nee requirement within the specified time interva shalla
LCo. As a failure to meet the operability requirement for an
uch the failure to perform Surveillance R irement
4.6.1.3.a fk a,ll the CIVs within the surveillance pari (i.e.
days plus the 25-percent extension) would have co tituted ,an 31
inoperable con' ition of the CIVs.
The oncoming USS
determine if the stified that he lacked sufficie information to
omplete surveillance had n been performed
within the survalliance frequency because he w
the
circumstances under which the surveillancenot
performed.
familiar with
procedure was
Furthermorg, he lacked sufficient information in the
control
had beenroom to deterni
performed withine if the complete. surveillance procedure
his experience, the CIV su he surveillance ' period. On the basis of
eillance was mormally performed in its
entirety; therefore, the potential existed that another partial
surveillance
CIVs. Although procedure had verified the position of the missed
the control room,previously performed surveillances were filed in
neither controlled these records' era
nor complete. ' for information only and were
'
The USS indicated that the previou stwo monthly surveillances on
the CIVs obtained from this ' file sqre performed incompletely;
however, he did not know whether surveillances on the missed CIVs
had been performed completely under \some other surveillance
procedure.
This was confirmed when tNe team interviewed the
surveillance coordinator! Who indicated that approximately once a
missed surveillances were performed under different tasks. mo
Upon identificatiop/ \
of the potential missed surVtillances the USS
had actually b en missedtoand,
initiated an inveftigation determine whether the surve,illances
concurrently, r -performed the
surveillance
the discove w hin three hours. The inspection tea verified that
time at whi time on the deficiency card correctly flected the
had been p it was verified that the previous two s elllances
formed incompletely.
Cone sion
,
On the basis of the testimony of the USS, the inspection te
neluded that the allegation was not fully substantiated becaus
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USS did not conceal the true discovery time of the sis CIV
surve ces to avoid a unit shutdown. The USS indi that he
'
was not pre ed to keep the plant in operation o prevent NRC
notification. stated that he had er been given any
indication or instruc to do " wha r it takes" to kecp the
unit on line or to avoid N t ation of unusual events. The
USS did not know and co no onfirm if the previous CIV
surveillances had been equately per ed and believed that the
surveillance co re-performed within allowable outage
time; ther , his actions to initiate an invest on into the
4
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adequ of the previous surveillance and to concur re-
ora the CIV surveillance procedure were appropriate.
- : ":f: chance 9fth Inemable source -Jtanae- Monitor Mucien
f Instrument
1
1 An al gation indicated that the operations staff allege
'
knowing violated Technical Specifications (TS) when the uni as
taken fro Mode 5 (cold shutdown) to Mode 6 (refueling) th a
i
source rang monitor (SRM) nuclear instrument inoperable d that
the prohibite operational mode change was made in orde o reduce
the critical pat outage time.
! Discussion
i
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The inspection team rev ved the documentati of the mode change
' described in Licensee Eva Report (LER) 90 04 for which non-cited
Violation 50-424/90-10-03 s issued. e LER indicated that TS 3.0.4 was violated on March 1990, en Unit 1 entered Mode 6
from Mode 5 with an 140 for Sou e Ra .ge Channel IN31 in effect to
allow performance of an 18-mont 'hannel calibration. The LER
indicated that the root cause to t avant was personnel error by I
the shift superintendent.
The inspection team confir'med that TS 310.4 required that entry
i into an operational mode not be made unlesssthe conditions for the ;
'
. LCO are met without aeliance on the provisions of the action
requirements. With.one source range monitor inoperable, TS 3.9.2,
" Instrumentation,' could not be satisfied in\ Mode 6 without
reliance on the' action statement.
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/
Personnel w[re interviewed to (1) confirm the effect on the outage
scheduled /irectly attributed to this TS violation, (2) etermine
whether'it was known at the time of the mode change that mode-
i restraining LCO was in effect, and (3) determine the exte t of
,
phasis on schedule.
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The testimony and a review of the outage schedule confirmed tha (
ere was a reduction in critical path outage time which w !
- d the l
! SRM ectly o anattributed
operable status. to proceeding to Mode 6 before restoring /
i l
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l The te isony also indicated that the shift superintendent (SS) and
{ .the uni shift supervisor (USS) did not recognize that 'a mode-
j restrain LCO was in effect at the time of the mode change. Both
!
the SS and SS were aware that there was an active 140 on the SRM,
,
but neither f them had connected the LCO to the mode., restriction.
i
i
contributing ctors to the error were that both th 8 and USS had
directed their attention to a problem with the esting of the :
) engineered safet features actuation system (ES ) sequencer and i
i that the-work whi had been emphasized to be 1 ding up the mode !
<
change was the d ontamination of the redctor head. Upon i
j notification that th Health Physics Department had cleared the l
reactor head for work, the SS granted permission to enter Mode 6. i
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The testimony also indic
unreasonable emphasis on t
ed that there 'was no indication of an ;
critical path schedule. Both the SS ;
-
and USS indicated that they had never been given any indication or '
!
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instruction to do "whatever i takes" to stay on schedule. They
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also indicated that they did t , feel undue pressure to stay on
schedule and, particularly, not , f it meant compromising safety.
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The SS admitted that he was initia ly commended for the schedule '
j benefits; however, the violation of he Technical Specifications
'
was not recognized at the time. Thg SS indicated that he had .
- initially received some sitive fee ack during the morning
! management briefing for a shift's acco lishments and later in
! the briefing the TS vio ation was recognize and discussed. In the
l SS's opinion the re nition of the TS olation negated all ,
- positive feedback.
a
] The inspection t an identified an additional c cern during the
inspection conc ning the format and use of the
'
status sheets.
On the basis interviews with the SS and USS a the review of
- the format o the 140 status sheets, the inspection as concluded
i that both a format and normal use of this form co ributed to
this TS v lation.
i
j
The LC status sheet, is a two-sided form; the section for quired
actio a begins on the front and continues on the back, who the
- "re rks" section is located. During the testimony, both t
i an USS indicated that their usual practice, notwithstanding a SS
e
anges, was to review only
restorative actions were noted on the back. In this case, the mode
the front of this form because onk
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!
seestraint
ion. was noted on the back of the form in the " remarks" ,
l
LER 90 4 did not identify the format and use of the LCO st us
sheet, as cause of the violation therefore, corrective ions
,
have not ye een i:aken in this regard. The failure to dentify ,
and implement dequate corrective actions to preclude repetition is
a violation of l'O.CFR 50, Appendix B,
Actions," and as s(uch will be followed as: Criterion XVI/ " Corrective
VIO 50-424/90-xx-03, "F
,
s
ure To Determine and' implement Adequate !
Corrective Actions." '
!
Conclusion N j
!
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,
onthebasisofthetranscribed,Jnkerviewsandfromitsreviewof
the outage schedule, )
the i pectionsteam concluded that the
allegation was not fully s stantiated. N.The testimony indicated ;
'
that the mode change w a critical pathsites. However, the
testimony of the shift
perintendent and the unit shift supervisor
involved indicated that at the time of the mode' change they were
not aware that an'Ir0 was in effect on the SRM a that a mode
change was pro ited.
The ins
the ion team also concluded that the corrective act
failed to identify that the format and use of thns for
140
sta sheets, was one of the causes of the event. Therefore, e
f
ure to implement appropriate corrective actions was found to
,
violation of 10 CFR 50, Appendix. 8, Criterion XVI.
2.b pr Backdatino of sianatures
An allegation indicated that a temporary change to Abnormal
Operating Procedure (AOP) 18028-C, "Ioss of Instrument Air," was
not approved within the 14-day requirement of TS 6.7.3.c; and that
the unit superintendent intentionally incorrectly signed and dated
the
'
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temporary change to indicate that the TS requirement was
satisfied.
j- Discussion
TS 6.7.3.c requires that temporary changes to AOPs which do not
4
involve changes to the intent of the original procedure be
documented
within 14 days and
of reviewed in accordance with TS 6.7.2 and approved
implementation. TS 6.7.2 requires that changes
to AOPs be reviewed as stated in administrative procedures and
approved
Administrative by theProcedure
Plant Review Board (PRB) and gener11 manager.
00100-C, "Cuality Assurance Records
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j Administration," Paragraphs 4.1.1.4 and 4 .1.1. 8, require ~ that
'
i corrections to Quality Assurance records exhibit necessary and
- appropriate signatures, initials, and dates.
!
i operations Procedure 18028-C, Revision 7, provided operator actions :
.
in the event of a loss of the instrument air system. A temporary '
j change to the procedure was initiated on May 29, 1990, to delete
i the references to the header isolation at 70 psig and the
i associated actions. This change was processed in accordance with
- Administrative Procedure 00052-C, " Temporary Changes to :
i
Procedures," which allowed the temporary implementation of minor i
j
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changes to procedures as long as the change was approved by the PRB j
and signed by,the general manager within 14 days of the temporary
change. Therefore, Temporary Change Procedure (TCP) 1802-C-7-90-1
was required to be approved by the PRB and signed by the general
,
)
manager by June 12, 1990. '
l
'! The PRB tabled the TCP on June 8, 1990, (PRB meeting 90-81) and i
j assigned action to the Operation's Department to void the TCP or
revise the TCP to incorporate the PRB comments. Revision 8 to
] Operations Procedure 18028-C was developed to modify valve numbers
- and descriptions reflected in Temporary Modificatiors 1-90-006 and
i 2-90-002. This revision superseded the changes of the TCP. On
i June 12, 1990, the PRB approved Revision 8 (PRB meeting 90-82) and
!
the TCP was removed from the control room copies of the procedure.
] On June 15, 1990, the unit superintendent lined out the operations
.
manager's previous approval of the TCP and marked the TCP form as
! disapproved by the operations Department. The date entered on the
! form was June 12, 1990.
I
j On June 22, 1990, the PRB secretary initiated Deficiency Card (DC)
1-90-282 which indicated that the unit superintendent incorrectly
i
dated the TCP with the date of June 12, 1990, rather than actual
j' was not processed within the required 14 days (i.e., by June 12,
,
1990). The resolution of these DCs, the associated PR8 meeting
i
minutes, and discussions with the operations manager and Nuclear I
Safety and Compliance Department staff indicated that described l
deficiencies were acknowledged and confirmed by the Operations
! Department on July 3,1990, and attributed to personnel error. The
I TCP form was dated with the date on which the Operations Department
l decided to void the TCP and not the date on which the original was
j actually signed. l
As part of the corrective actions for DC 1-90-282, a TCP record
,
correction notice was initiated to correctly indicate the date on '
! which the TCP fo11 was pro..ssed; however, tus TCP record
l,
correction notice could not be produced--one was subsequently
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4 written on August 14, 1990. In addition, the operations manager
- - counselled the unit superintendent and assigned him to investigate !
- both DCs because he was the most knowledgeable of the deficiencies ;
- and the assignment served to reinforce the reprimand. '
The
4
subsequent PRB meeting of June 28, 1990, (PRB meeting 90-90)
- determined that the 14-day TS violation addressed in DC 1-90-283
. was reportable to the VEGP vice president, but not to the NRC.
1 However, the inspection team found that the report to the VEGP vice
i president was not made.- On August 9, 1990, the PR8 (PRB meeting
}.90-104) confirmed that the report was required. As of August 17, !
i- 1990, ~ the licensee had not issued the required . cport to the VEGP
j vice president; however, the licensee intended to issue the report. >
,
With respect to the rationale for the unit superintendent's ;
actions, the inspection team learned (during discussions with the '
}. Technical Support Manager) that the PRB secretary told the unit
i superintendent on June 15, 1990, that the TCP needed to be voided
and 4 DC written for violating the 14-day requirement of TS 6.7.3.
l As discussed in Section 2.11 of this inspection report, Operations
i Department personnel are held personally accountable for violations
'-
and LERs (i.e., there is a direct impact on their bonus pay); ;
therefore, a reportable occurrence based on this event could have !
i
adversely impacted the unit superintendent's salary.
l
l The testimony of the unit superintendent indicated that he dated
- the TCP with the date (June 12, 1990) on which the PR8 disapproved
I it and not the date on which it was actually signed (June ' 15,
i 1990). Additionally, the unit superintendent had no recollection
l of any discussions on June 15, 1990, regarding violation of the 14-
l day TS requirement. He indicated that he never considered the 14-
day requirement despite his previous knowledge and training
i
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concerning this requirement and the June 12, 1990, expiration date
indicated on the TCP form.
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The testimony of the PRB secretary indicted that during a
!
' discussion with the unit superintendent on June 15, 1990, she ;
identified the need to void the TCP, as well as the need to write '
!. a DC for violating the 14-day TS requirement. Therefore, the
- inspection team was concerned about whether the TCP was voided
j' before or after the PRB secretary identified the need to void the
!
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TCP and initiate a DC. In order to resolve this discrepancy, the
inspection team discussed the discrepancy with the PRB secretary on
,. August 16, 1990. In addition to earlier testimony, the PR8
secretary indicated that during her discussions concerning the TCP
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with the unit. superintendent on June 15, 1990, the unit
superintendent had indicated that the TCP had already been voided
j aar13 : in the day.
,
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- conclusion
i
l On the basis of the testimony, the inspection team concluded that
- backdating to avoid a violation of the 14-day TS requirement was
I not '0117 ="h-"-ti tted T= idditi^=, the r^ cer- th t ibis
i practice m- a plant-wide problem,==- et *"11 y =nh=* =-t itt ed .
i However, the inspection team did confirm that TCP 1802-C-7-90-1 had
! been dated incorrectly; this was a violation of Administrative
i Procedure 00100-C, " Quality Assurance Records Administration,"
! Paragraphs 4.1.1.4 and 4.1.1.8 and will be followed as:
! 19-l's tq -G
' VIO 50-424/90-xx-@2' and 50-425/90-mm-er, " Failure to Establish or
Implement Procedures for Required Activities." \ 1
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<
g y Reportability of Previous Enaineered Safety Features Actuation
System Load Seauencer outaaes !
An allegation indicated that the operations Department incorrectly l
used a 72-hour shutdown requirement when one of the two ESFAS load
- sequencers was previously inoperable. It was also indicated that
l VEGP had taken no action to ensure that the past occurrences were ,
l identified and reported to the NRC as required by 10 CFR 50.73,
j despite newly acquired information that deenergizing an ESFAS i
.
sequencer required entry into the 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> limiting condition for
l operation (Iro) action requirements of TS 3.0.3. In addition, the
- possibility existed that the 140 for TS 3.0.3 (i.e. , 7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br /> to hot
. standby) were exceeded when the sequencers were previously
i deenergized for maintenance and testing. This concern was based on
(1) the lack of a specific TS for the sequencers, (2) the '
- operations Department historically linking the sequencer outages to
! the emergency diesel generator (EDG) 140 of TS 3.8.1.1.b (78 hours9.027778e-4 days <br />0.0217 hours <br />1.289683e-4 weeks <br />2.9679e-5 months <br />
, to hot standby), (3) a limited review of past maintenance work
i orders (MW0s) indicated possible sequencer deenergiration; and
'
(4) comments by the engineering staff that the sequencers had been
previously deenergized.
Discussion
l There are two ESFAS sequencers for each unit--one for each 4.16-
e kilovolt (kV) emergency bus. Each sequencer is activated by one of
! two conditions, undervoltage (UV) on the associated emergency bus
! or a respective train's safety injection (SI) signal. Upon receipt
i of either or both of the initiating signals, each sequencer will
j perform all or part of the following functions:
' '
Start the associated EDG.
I
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j Stop any test sequence in progress.
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Strip the associated emergency bus of all loads (UV j
i only).
close the associated EDG breaker (UV only).
[ Energize the associated train's engineered safety
features (EST) loads as determined by the initiating
j signal.
l Each ESFAS sequencer contains three levels of UV detection and
j
system response, as well as the power supply for this UV circuitry.
Four potential transformers monitor the emergency bus voltage for !
} these three levels of degraded bus voltage (Invel 1, 5 70 percent: l
- Level 2, 5 86 percent; and 14 vel 3, 5 88.5 percent) and furnish an ;
- analog signal to three sets of four bistables located in one of the
4-
.
five sequencer cabinets.
!
Level _1 is the " loss of voltage" and Level 2 is the " degraded
!
i
voltage" which is referred to in TS Table 3.3-2, Items 6.d, 8.a.
and 8.b. As these TS items (applicable in Modes 1 through 4) do
i
not address the loss of all four channels in Level 1 or in Level 2
i
(as would be the case when the sequencer is deenergized), TS 3.0.3
would apply if such a loss were to occur. It should be noted,
i
however, that if the sequencer were deenergized, it could not
respond to a safety injection signal either. Therefore, there
would be only one automatic safety injection actuation channel
! (i.e., associated with the unit's unaffected sequencer) and Item
i 1.b of TS Table 3.3-2 (6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> to hot standby) would be the most
l- limiting 140. 1
'; Discussions with the operations manager, the assistant general i
,
manager-plant support, and system engineers for the ESFAS and !
i sequencers confirmed that the Operations Department historically '
2
linked the sequencer outages to the emergency diesel generator
(EDG) 140 of TS 3.8.1.1.b (78 hours9.027778e-4 days <br />0.0217 hours <br />1.289683e-4 weeks <br />2.9679e-5 months <br /> to hot standby) . Although the )
!
applicability
had
of TS Table 3.3-2 and TS 3.0.3 to sequencer outages l
l been recently identified, past sequencer outages were not
- reviewed. Therefore, with the assistance of the licensee, the ;
i
inspection team reviewed the completed MWOs which were performed on '
4
the sequencers on Units 1 and 2, as well as the related
i
1
Instrumentation and control (I&C) , Engineering, and Operations
Department surveillance tests.
-
,
)
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The review of completed MWOs did identify several instances where
the work performed would most likely require the sequencers to be
,
deenergizedt however, the associated unit was found to have not
.
been in Modes 1, 2, 3, or 4 at the time the work was performed.
.
Somewhat = related to this concern, the review did identify two
4
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occurrences (March 4 and June 17, 1987) where the Unit 1 Train B
l sequencer was inoperable during the change of sequencer controller
4
card A (SI4T A4-3) . Specifically, when the controller card was
j removed, both the automatic SI function and UV function for the
sequencer were rendered inoperable. Because the unit was in Mode
i 3 (hot standby) during these two occurrences, the sequencers and
the ESFAS were required to be operable per TS 3.3.2. However, the
i associated 140 status sheets (1-87-354, dated March 4, 1987 and 1-
I
87-566, dated June 17, 1987) only recognized TS I40 3.8.1.1.b as
being applicable to the outage. Despite the fact that 140s
,
associated with TS Table 3.3-2 (Item 1.b) and TS 3.0.3 were not
-
recognized, these TS were not violated since the system was
j . restored within 30 minutes and 10 minutes, respectively, f1F
i ' fditie , 2- ran unit rerrin:d in 5:t Ot:nry, pert:tility "adar
_
4
j *^ 07 00.72 w 00.73 :: n;t r:';;ir:d [i.:., there t' : pr:r !
.
r=A n<-+ 6 ihil: 1. 2 TS LOO (10 OFP 50.?2) ner we G. piani.-aken I
j te hat utandhy er : :::Olt ;f e TO LOO (10 m 50. H ) F. 1
,
i
similar to the MWO review, the inspection team's review of related
I&C, Engineering, and Operations Department's surveillance tests
l did not find any examples of the sequencers or the ESFAS being
l deenergized in Modes 1 through 4. Completed 18-month ESFAS channel
i calibrations, EDG tests, and ESTAS tests were verified as having
i been done in Modes 5 and 6. Completed quarterly testing of the
i ESFAS Auto SI K610 slave relay, which removed the automatic SI
signal to the sequencer, were verified to be performed within time
i limits allowed by TS 3.3.2. All other sequencer testing that used
l installed test circuitry is automatically bypassed on an SI or UV
- signal.
4
i
In addition to the inspection team's review of MWos and ,
l surveillance test procedures, the system engineers for the l
i
sequencers and ESFAS [as well as the nuclear steam supply system l
- (NSSS) supervisor) were asked if they knew of any time in which the l
4- sequencers were deenergized in Modes 1 through 4. None of these '
)
engineers remembered any such occurrences.
'
A review of applicable operator treining material (System
1
l
.
' Description 8b for Engineered Safety Features System Sequencers)
revealed that there was no reference to ESFAS TS 3.3.2, just those
for the diesel and other power sources and distributions (i.e., TS
i 3.8.1.1, TS 3.8.3.2, TS 3.8.2.1, TS 3.8.3.1, and TS 3.8.3.2.).
This finding, along with the March 4 and June 17, 1987, occurrences
l discussed above, indicates that the operations Department
historically has not linked sequencer outages to the 140s of TS 3.3.2 or TS 3.0.3. Nevertheless, discussions with the operations
,
~ manager and the licenced operators on shift indicated that although
no written guidance or TS interpretation existed for the
,
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- sequencers, the operations Department staff would currently !
consider all applicable TS requirements, including TS 3.3.2 and
j 3.0.3.
! Conclusion
- The 140 actions of TS Table 3.3-2, "ESFAS Instrumentation," are ;
'
] applicable for determining the operability of ESFAS components;
'
however,-if a load sequencer is not operable, the more restrictive i
requirement of TS Table 3.3-2, TS 3.0.3, or the affected system Iro
i should be considered. Although the EDG LCO of TS 3.8.1.1.b had ;
- '
been used for sequencer outages in t.he past, the allegation's ;
concern of possibly exceeding the 140 for TS 3.0.3 when the :
.
sequencers were previously deenergized yM * not 5: ';11y ,
} c'2:t: .tiatad. loa!nR*1co.
} Because there is no specific TS for the sequencers and considering ,
j (1) their unique interaction with numerous other systems and ;
j equipment, and (2) the varying degrees in which related failures, !
i maintenance work, and surveillances can affect the sequencers' :
j associated functions, the inspection team concluded that additie.31 !
guidance for the operators is warranted. Therefore, this issue l'
l
,
will be followed as an inspector followup item pending further
review and evaluation and is identified as -
I
N-If 39- 6
- IFI 50-424/90-M and 50-425/90-xm-94, "Iack of Operator Guidance I
1
concerning the Leo Actions Applicable During ESFAS Sequencer '
outages."
1
- .- 2:11211!ty -' h-==~ v nine.1 r:eneratera
{
i An allega n indicated that VEGP counted the number of starts
e failures o e EDGs incorrectly and misrepresente is
l information know in (1) a verbal presentation to C, (2)
- a formal response to Region II confirmation o ction letter
l (CAL), and (3) LER 90-00 , evision 0, issued owing the March
j- 20, 1990, event involving fa es of the f1A. In addition, it
j was alleged that VEGP attempte use the EDG reliability
- issue with Revision 1, and delayed . -006, Revision 1, in order
j to avoid drawing attention to ese inco et representations.
1-
i
Discussion
]
The spection team reviewed the following:
i
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w--, . --w vge ~ _ -
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,
!, 1) VEGP presentation in the Region II office ~ on April 9, 1990
- concerning the site area emergency event of March 20, 19 .
his presentation is identified as Enclosure 2 to the Re on
i meeting summary letter of May 14, 1990. /
1
4
~2) VEG 1etter dated April 9, 1990, in response to the Region II
i cont ation of action letter (CAL) dated March 23,'1990. }
} !
j 3) LER 90-006, issued April 19, 1990, to report the site area
emergen event of March 20, 1990. >
i These documentsMnd the following procedures describe the EDG
- operability.statu and the licensee's program for recording EDG
! start information and the EDG surveillance test frequency i
4 requirements:
\
Procedure 550 8-C, " Diesel Start.Ing" l
?
'
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Procedure 1314 -1, "EDG Operation for Maintenance
Troubleshooting Maintenance Testing"
^
Procedure 14980-1, EDG Operability Test" i
e
l The licensee indicated in a tran
\/arency used during the Region II
l presentation that there were 18 s cessful starts on EDG f1A and 19
i
' successful starts on EDG $15 tyeen the loss-of-offsite-power
-
event (March 20, 1990) and the pXesentation to Region II of
April 9, 1990. The inspectiop' team r iewed the EDG start logs and
j the detailed EDG start records complet during the performance of
i Surveillance Procedures 13145-1 and 1498 -1. The inspection team's
i review of these records in'dicated that th a were 31 EDG f1A and 29
'
EDG #1B attempted startpi Two of the EDG A and eight of the EDG
f1B starts involved pr#blems or failures. EDG f1A there were a
i total of 29 successful starts and on E 013 there were 21
i successful starts. However, there were s veral intermittent
- problems or failurm/ s during the EDG f18 start tempts. Although
! there were 29 6 sequential starts n EDG f1A, the
- inspection team,7identified
ccessful, that there were on1 12 successful,
j sequential staits of EDG $15 during this time peri .
i
! TS 4.8.1.1. .a requires that each EDG be demonstrate operable in
l accordane with the periodicity specified in TS Tabl 4 . 8-1 by
l' Verifyl that the EDG starts and assumes rated fra ency and ,
voltage in accordance with the EDG surveillance test This
- . surve lance test required a minimum run time of 1 hou at a
l .desi ated load. The inspection team found that at the time the
l pre entation to the NRC, the operability test of the EDGs had een
s cessfully demonstrated two times. In addition, the EDGs ad
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i uccessfully passed four operability tests before Unit i entere
j e 2. Therefore, the EDGs were reliable and operable before t e i
j presentation.
/
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The WRC Region II Office was not verbally informed of the l
j
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incomp'lete information regarding the number of EDG starts until
1 June 11 1990 (approximately 2 months after.the presentation). .
j Although evision 1 of LER 90-006, dated June 29, 1990, correctly !
) identifiedsthe number of sequential, successful EDG starts from the i
j and of the'saintenance test program (i.e., the first successful
! operability st per TS 4. s . l .1. 2 a ) until the issuance of LER 90-
i 006, Revision , dated April 19, 1990, this revision (June 29,
j 1990) did not address the number of EDG starts that should have
- been cited in th presentation, in the VEGP letter in response to
the CAL, and in R 90-006, Revision O. The correct number of ,
j sequential, ' success ul starts for EDG #18 was 12 and not 19 as !
! indicated in the pres tation. Therefore, the NRC was not informed l
of the correct informa ion in a timely manner. 1
The information presente to the NRC did not coopletely describe
. the problems and failures k at occurred with EDG $18. However, the '
i testimony indicates that t general manager's intention was to
i demonstrate that the problem involving the immediate trip of EDGs
identified during and follow gfthe March 20, 1990 event were
corrected prior to Unit 1 start .- Therefore, a compliation of the
- total number of successful sta' s (i.e., a start that did not
s
ortan factor in his presentation.
i immediatelytrip)wasanimp/
l The testimony also indica d that e unit superinten: lent (Us) i
-
researched the EDG starti history fo the NRC presentation based
- on a request from the ge ral manager. e general manager did not
- ask the US to prepare a complete descri ion of the EDG starting
i history. specifica11 ' the general manage requested a summary of
l only the successfu starts--the informati concerning the EDG
j problems and fallu s was not requested. In ddition, the Us used
j the unit reactor rator logs instead of the E operating logs to
- compile the EDG tarting history. The reactor perator logs did
! not contain a etailed description of problems failures which
! occurred dur g the EDG starts. The US did not ceive specific
j guidance co erning the type.of EDG starts that he w requested to
l
summarise. In addition, the testimony indicated that the original
, assumptigns and EDG $1B start information used in the esentation
were alp 6 used in the VEGP response to the CAL, and in R 90-006
issuedApril 19, 1990.
, i
.
Thef [nspection team's review of ' the Unit 1 EDG's reliabil and
o rability status between March 21 and June 14, 1990, raise the
11owing additional concern. The review was performed to ve fy
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t at all EDG failures were identified and classified as eit
va id or non-valid and were reported to the NRC as required b TS
r
4.8. .1.3 and TS 6.8.2. The inspection team discovered tha the
foll ing f ailures during starts of EDG f1B had not been clas ified
as val d or non-valid and, consequently, had not been repofted to
the NRC ursuant to TS 4.8.1.1.3 and TS 6.8.2.
EDG S art Date Remarks
/
1-90-13 3/22/90 EDG trfp, high-
temperature lube oil.
Ma i n 't e na nce
troubleshooting test.
/
1-90-134 3/23/90 EDG / trip, low jacket
water pressure.
M ,4 i nt a nance
2 troubleshooting test.
.
1-90-136 3 24/90 EDG intentionally stopped
due to alarmed condition,
high jacket water
temperature. Maintenance
troubleshooting test.
1-90-157 5/23/ 0 EDG trip, high jacket
water temperature
M a i nt e na nce
troubleshooting test. i
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1-90-160 5/23/90 END G trip, 1ow
tutbocharger
-161 o i' pressure.
Main nance
-162 troub e. shooting test.
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1-90-164 5/23/90 EDG trip high jacket
water
-163 temperature. Maintenance
troubleshoot g test.
I
These in .ction findings were discussed with the e ineering l
support anager who agreed that these types of failures ave not '
been ported. The licensee committed to have all E start I
,
recor s reviewed for any unreported failures.
Th inspection team also four.. that a violation -as previou ly
i entified for the failure to report all EDG failures in Inspecti
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, Re rt 50-424/87-57 dated November 1987. Although the failur to
,
repo all EDG failures is a violation of TS 3.8.1.1.3
6.8.2, the inspection team concluded that the failure
d TS
' s the
result inadequate implementation of corrective a ions to
j
l
prevent re urrence of a violation and, as such, is a vjdlation of
- 10 CFR 50 Ap ndix 8, Criterion XVI, " Corrective Actiop," and will
be followed a
VIO 50-424/90-xx- , " Failure to Determine and Implement Adequate
j Corrective Actions. ,
,
/
j Conclusion
1
/
/ l
i The. allegation that VEGP i orrectly counted the number of starts
l
. reliability in order to s1 cad the NRC was partially l
. substantiated. On the basis of u sworn testimony and its review
j j
of EDG records, the. inspection te concluded that the Region II 1
,
presentation was not intended to r resent a specific number of
j successful valid tests as specified in G 1.108 and TS 4. 8.1.1.2a, l
i
but rather to describe the EDG maintenan test program and the EDG ,
! reliability status. Nevertheless, the i ction team concluded !
i
that the NRC was not informed of the incor et information until
the NRC asked for it dh[ ring the inspection. l
e lack of specific I
- guidance concerning he EDG information desi d, coupled with
- inadequate researc !
of the EDG starting histo , resulted in 1
providing incomp te and therefore inaccurate infotsation to the ]
NEC. The CAL r ponse and LER 90-006 were also inco ct because
- they were bas on the IDG start information that was c iled for
! the VEGP pr antation in the Region II Office. The inspec on teaa
! concluded at the failure to provide accurate information o the
] NRC was a violation of 10 CFR 50.9 requirements and wil be
l follow as: .
l VI 50-424/0-xx-05; 50-425/90-xx-05, " Failure to provide Accurate
,
r
ornation to the NRC."
, 7 6 y Air Quality of Emeraency Diesel Generator Startina Air System
\
An allegation indicated that VEGP had no basis for its conclusions
i regarding the air quality of the EDG starting air system and
misrepresented the air quality in the licensee's written response ,
- to the CAL.
I
f Discussion
i
i
The ir. pection team reviewed the maintenance records and deficiency
- cards associated with Unit 1 EDG starting air system. The team i
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4
was established when preoperational tests were init
on Unit 1 in November 1986. t
' this date, '
part of 1988,but' not on a scheduled frequency.During Dewpoint themeasurements
latter w:
!
i established to measure the EDG starting air system The
dewpoi{
!
the
current air drPM progran required checking the dewpoint monthly, cleanin !
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i
addition, yer condensing
operating units,11882-1,
Procedure and cleaning the fan motors. In
i "Outside Area Rounds," i
i dryers
noisture. be blown down on a daily basis untilrequired that the E)
i
they were free of
operators blev The inspection team verified that the plant equipment ,
performance of their down the air systems on each shift during the
rounds.
!
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A review of the Unit 1 EDG maintenance history records indicat e
d
.
that the majority
specifications. of the devpoint
There were instances, measurements taken were n
withi i
j
i asasurements were above specifications.however, when the dewpoint i
primarily
instruments, attributed to problems with (1) These conditions were
l
extended pwriods (2) ofsystem
time, andair dryers beingthe dewpoint measuring
system following maintenance. (3) repressurizing the EDG air start
out of service for I
i
s
The inspection team reviewed maintenance records associated an
with
internal inspection of the EDG air start system air receiver5-
micron control _ air system filter inspection and replacement ,
the replacement of the dowpoint measuring instrument, with and
analyzer. an EG6 ;
i
- Following the loss of offsite power event of March 20 G
1990, the control air system instrument lines were disconnected or
,-
f
maintenance troubleshooting and functional tests of Calcon sensors
The system engineers associated with this work stated that no .
i
- evidence of internal noisture or corrosion was noted
inspection and calibration of the calcon sensors or theair cortrol
during
system instrument lines when this equipment was disconnected for
.
!
maintenance troubleshooting and testing.
j Conclusion -
'
!.
The inspection team concluded that the licensee did have an
{'
adequate basis to assess the quality of the EDG starting air
system. ,
1
inspection
addition, the of EDG air start system components a on. In
for degr
i PM program dewpoint readings have shown more
i
The
concerning allegation
EDG air
that
start
system
did not have a ements
aer.basis for th
-4.i.uil-i A C #id *4 C D quality was not
y -M4y
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um * A INhgebm.
yQWidLC. L m. eta & Guy as@v
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- M
y Reportability of Previous System Outages l
f
!
An allegation indicated that VEGP failed to immediately notify the \< >
{
j
NRC as required by 10 CFR 50.72 when VEGP identified that both
trains of the containment fan coolers (CFCs) had been previously
inoperable at the same time on Unit 1.
i
j
.
I Discussion
i
i.
I
The inspection team's review of plant records indicated that this !
! condition occurred when EDG f1A was declared inoperable when tape
(used when the EDG was being painted) was found on the EDG fuel
j rack. The tape kept the fuel injector piston from moving and
i injecting fuel into the EDG. With EDG f1A inoperable, the
.
equipment associated with the Train A was also inoperable. In the
process of investigating the installation of the tape, VEGP !
i;
identified that this condition existed during a period when the
Train B containment fan coolers were also in a degraded condition :
j for maintenance.
i
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During the performance of Surveillance. Procedure 14623-1, Train B
!
1
containment
speed. 140 1-90-560 fan cooler (CFC) 1-1501-A7-003 failed to start in slow
was initiated at 0115 hours0.00133 days <br />0.0319 hours <br />1.901455e-4 weeks <br />4.37575e-5 months <br /> on June 19, 1990,
J and maintenance on the CFC was initiated. The CFC was returned to
j operable status on June 19,1990, at 1415 hours0.0164 days <br />0.393 hours <br />0.00234 weeks <br />5.384075e-4 months <br />. Approximately 9
hours later [on June 19,1990, at 2359 (Lco 1-90-562)), EDG f1A was
i
determined to be inoperable because the tape had been installed on
i- the fuel rack. On July 17, 1990, VEGP issued LER 90-014 to
j
identify the previously unrecognized violation of the 140 in
- accordance with 10 CFR 50.73.
'
, Conclusion
!
Based upon the fact that VEGP did not become aware that both trains
,
of CFCs were simultaneously inoperable until after the Train B CFC
!
j fan had been returned to service, the immediate notification
requirements of 10 CFR 50.72 were not applicable. The allegation
, that previously
the VEGP failed to immediately
degraded c notify the NRC upon discovery of
- e , - ,ondition> .
of the CFCs was not .Se44y
j
g.1 W Intimidation of Plant Review Board (PRB) Members
i
i
f An allegation indicated that Plant Review Board (PRB) members were
allegedl
j meeting.y intimidated and pressured by the general manager in a PRB
The meeting occurred in February 1990, to determine the
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acceptability of the safety analysis for the installation of the
FAVA microfiltration system.
Discussion
T.i j
k
As discussed in Section ht" of this inspection report, several ,
!
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safety evaluations were performed for the installation of a
temporary modification which installed the FAVA microfiltration
i system. Discussions with PRB members indicated that during the
t review of these safety evaluations, various PRB members had
1 expressed reservations on several occasions concerning the
4
acceptability of the installation of the FAVA system.
!
.' Despite these reservations, the inspection team's review of the PRB
- Meeting minutes associated with this temporary modification
j
identified few instances of the PRB members documenting their
i dissenting opinions. Specifically, PRB meeting 90-15 (dated
February 8, 1990) documented one PRB member's negative vote and
'
i dissenting opinions regarding the acceptability of exempting the
temporary modification from regu'.atory requirements and the
, adequacy of the system's safety evaluation. PRS Meeting 90-28
. (dated March 1, 1990) indicated that information and issues
regarding the FAVA system's safety analysis were presented to the
j PRB and that the general manager solicited written comments and
! questions from other members for resolution. The only other
l example was in PRB meeting 90-32 (dated March 6, 1990) which
!- identified a dissenting opinion related to the acceptability of
j votina on the FAVA system installation when the PRB member who ;
- raised the initial questions and concerns on the operation of the
i FAVA system was not present.
! Discussions with the PRB members indicated that during the various
PRB meetings concerning the installation of the FAVA system, the ;
i PRB members felt intimidated and pressured by the presence of the '
l- general manager at the PRB meeting. The sworn testimony confirmed
4
that on one occasion an alternate voting member felt intimidated ;
- and feared retribution or retaliation because the general manager i
j was present at the meeting and the PRB member knew the general 1
j. manager wanted to have the temporary modification approved. ;
j However, the testimony also indicated that the.PRB member did not '
a
alter his vote and felt comfortable with how he had voted. In
l addition, the PRB member was not aware of any occasions on which he
or any other PRB member had succumbed to intimidation or feared ;
i
! retribution.
!
'
The incpection team verified that the general manager was informed l
i
following this meeting that several PRB members viewed his presence
- as intimidating. As a result, on March 1, 1990, the general
,
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manager set with all PRB members to reiterate the member's duties
and responsibilities.
He specifically told the members that his
presence at PRB meetings must not
influence them and that !
alternates should be
responsibility. Heselected who would feel comfortable with this
also addressed i
the difference between
and their respective methods for resolution. or quality concerns,
professional differences of opinion and safety
conclusion ,
The inspection
felt intimidated
was present at the andPRB team
feared retribution
meeting. concludedbecause the that general in manager
on* case a PRl
However, this member 6ala nor W
change his vote in response to this pressure and the general
manager met with the PRB to allay fears. Based on the testimony,
the inspection team concluded that retribution did not occur. i
Nevertheless, this confirmed event and the absence of dissenting '
opinions in the PRB meeting minutes indicate that there was a '
potential for an adverse affect on open discussions at the meeting, t
The licensee needs to ensure that PRB members freel
express their technical opinions and safety concerns.y and openly
K Personnel Accountability
As a result of several comments and questions by the licenced
operators
to rate theto the inspection team, the team reviewed the method used
supervisors. performance of the shift superintendents and unit shift
Discussion
The o
rations manager stated that the shift superintendents (SSs)
"
e SSs re ed to su int ndent
i s and a
US personally prepared the performance appraisals of the 8 s.
i The personnel accountability system, first used in 1989, was a pay-
for-performance methodology. Annual pay increases and e percentage
i of
in the Operations Department
accountability categories. bonus were dependent on their ratings
,
i
subdivided into performance categories.Each accountability Most of the performance category was !
categories vern based upon group performance.
.
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eliminated, any differential in pay will Once these are i
- result from eight
t
performance categories. Implementation of the plan in 1989 could
i result in
superintendent. up to an $8,000-a-year difference 'n bcnus pay to a shift
weights are: The performance categories and their relative
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Personnel safety 4.1%
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Regulatory compliance 10.2%
.
ESFAS actuation 12.2% }
I Reactor trips 10.2%
!
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- MWO performance 4.1%
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Special projects a.2% '
=
Personnel development 30.6%
l .
Training 20.4%
,
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{ Therefore, 51 percent will be associated with personnel development
]
and training and 32.6 percent will be associated with the number of
- LERs, and violations (i.e. , regulatory compliance (10.2 percent), ;
.
ESFAS actuation (12.2 percent) and reactor trips (10.2 percent)]. '
Conclusion
'
The inspection team concluded that there was a
t
potential
'
,
disincentive for identifying items which may result in LERs or
violations.
'
In addition, the inspection team concluded that the
j operations manager
information to the inspection provided incorrect
team. or inadequately researched
!
i
The inaccurate information )
concerned whether the operations manager personally performed the
a
performance appraisals of shift superintendents. The information i
- -was not very important because the inspection team did not use the 3
j informationteam
inspection as the basis forthat
concluded a significant
this failure inspection finding. The {
-
to provide accurate ]
i information was an example of a violation of the 10CFR 50.9
{
requirements
followed as: to provide accurate information to the NRC and will be
' 14-1L- Ig-12.
,
VIO 50-424/90-aoeHPJ; 50-425/90.xx-65, " Failure to Provide Accurate
- Information to the NRC."
'
j 3.0 EXIT INTERVIEWS
1
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The inspection scope and findings were summarized on August 17,
i
1990, with those persons indicated in Appendix 2. The inspection
team described
inspection results.the areas inspected and discussed in detail the
The licensee made numerous
,
comments. dissenting
i
materials provided to or reviewedThe licensee did not identify as proprietary any o
i inspection. by the inspector during this
,
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.
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DRAFT - PREDECISIONAL INFORMATION
APPENDIX 1
LIST OF TRANSCRIBED INTERVIEWS
DATE TIME PERSON
,
8/14/90 904 hours0.0105 days <br />0.251 hours <br />0.00149 weeks <br />3.43972e-4 months <br /> George Bockhold
911 hours0.0105 days <br />0.253 hours <br />0.00151 weeks <br />3.466355e-4 months <br /> Jim Swartzwelder
1023 hours0.0118 days <br />0.284 hours <br />0.00169 weeks <br />3.892515e-4 months <br /> Harvey Handfinger
1026 hours0.0119 days <br />0.285 hours <br />0.0017 weeks <br />3.90393e-4 months <br /> Bill Diehl
1109 hours0.0128 days <br />0.308 hours <br />0.00183 weeks <br />4.219745e-4 months <br /> Mike Horton
1335 hours0.0155 days <br />0.371 hours <br />0.00221 weeks <br />5.079675e-4 months <br /> Mike Chance
1136 hours0.0131 days <br />0.316 hours <br />0.00188 weeks <br />4.32248e-4 months <br /> Jimmy Paul cash
1338 hours0.0155 days <br />0.372 hours <br />0.00221 weeks <br />5.09109e-4 months <br /> Dudley Carter
1529 hours0.0177 days <br />0.425 hours <br />0.00253 weeks <br />5.817845e-4 months <br /> Bruce Kaplan
1625 hours0.0188 days <br />0.451 hours <br />0.00269 weeks <br />6.183125e-4 months <br /> Greg Lee
1800 hours0.0208 days <br />0.5 hours <br />0.00298 weeks <br />6.849e-4 months <br /> Jeff Gasser
8/15/90 906 hours0.0105 days <br />0.252 hours <br />0.0015 weeks <br />3.44733e-4 months <br /> Allen Mosbaugh
937 hours0.0108 days <br />0.26 hours <br />0.00155 weeks <br />3.565285e-4 months <br /> Ernie Thornton
1009 hours0.0117 days <br />0.28 hours <br />0.00167 weeks <br />3.839245e-4 months <br /> John Gwin
1048 hours0.0121 days <br />0.291 hours <br />0.00173 weeks <br />3.98764e-4 months <br /> Steve Waldrup
1335 hours0.0155 days <br />0.371 hours <br />0.00221 weeks <br />5.079675e-4 months <br /> Jerry Bowden
1452 hours0.0168 days <br />0.403 hours <br />0.0024 weeks <br />5.52486e-4 months <br /> John williams
1637 hours0.0189 days <br />0.455 hours <br />0.00271 weeks <br />6.228785e-4 months <br /> Carolyn Tynan
1730 hours0.02 days <br />0.481 hours <br />0.00286 weeks <br />6.58265e-4 months <br /> John Williams l
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g 44 9
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DRAFT - PREDECISIONAL INFORMATION I
APPENDIX 2
PERSONS CONTACTED
Licensee Employees
- J. Aufdenkampe, Manager Technical Support
- G. Bockhold, Jr. , General Manager Nuclear Plant
- D. Carter, Shift Superintendent
J. Bowden, Work Planning ,
J. Cash, Unit Superintendent l
M. Chance, Senior Engineer, Engineering Support ,
- S. Chesnut, Technical Support i
C. Coursey, Mair.cenance Superintendent l
W. Diehl, Shif t Supervisor, Operations
Frederick, Safety Audit and Engineering Group Supervisor
,
- G. 1
J. Gasser, Shift Superintendent, Operations
- L. Glenn, Manager. - Corporate Concerns
- D. Gustafson, Maintenance Engineering Supervisor i
J. Gwin, Corporate Systen Engineer
- H. Handfinger, Manager Maintenance
- K. Holmes, Manager Training and Emergency Preparedness !
- M. Horton, Manager Engineering Support
.
,
B. Kaplan, Senior Engineer, Engineering Support
G. Lee, Plant Engineering Supervisor, Operations
- R. LeGrand, Manager Health Physics and Chemistry
W. Lyons, Quality Concerns Coordinator ;
- G. McCarley, Independent safety Engineering Group Supervisor
- C. McCoy, Vice-President, Georgia Power Company
- R. Mcdonald, Executive Vice-President, Georgia Power Company l
- D. Moncus, Outage and Planning ;
- A. Mosbaugh, VEGP Staff '
R. Odom, Nuclear Safety and Compliance Manager l
- A. Rickman, Senior Engineer - Nuclear Safety and Compliance i
- L. Russell, Independent safety Engineering Group, SONOPCO
- M. Shelbani, Senior Engineer !
- C. Stinespring, Manager Plant Administration
- S. Swanson, Outage and Planning Supervisor ;
- J. Swartzwelder, Manager Operations -
E. Thorton, Shif t Supervisor, Operations I
- E. Toupin, Oglethorpe Power Corporation .
C. Tynan, PRB Secretary i
S. Waldrup, Planning and Scheduling Supervisor
J. Williams, Shift Superintendent, Operations ,
- Attended exit interview, August 16, 1990. ;
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._..m , - , ., . , _ , , . . . _ _ ___..___._______________#
._. -. - - . -- - - . . _ . - _ . - - - . _ - - . _ _ . . ___
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DRAFT - PREDECISIONAL INFORMATION
APPENDIX 2
PERSONS CONTACTED (continued)
! NRC Employees Who Attended Exit Interview
-
R. Aiello, Resident Inspector - Vogtle
B. Bonser, Senior Resident Inspector - Vogtle
M. Branch, Senior Resident Inspector - Watts Bar
R. Carroll, Project Engineer - RIIK. Brockman, Chief, Reacto
i
N. Huneauller, Reactor Engineer - NRRL. Carner, Senior R
0. Matthews,
>
Project Director - NRR
J. Milhoan, Deputy Regional Administrator - RII
R. Starkey, Resident Inspector - VogtleL. Reyes, Directo
P. Taylor, Reactor Inspector - RII
M. Thomas, Reactor Inspector - RII
,
C. VanDenburgh, Section Chief - NRR
J. Wilcox, Operation Engineer - NRR
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- DRAFT - PREDECISIONAL INFORMATION
APPENDIX 3
LIST OF ACRONYMS i
AOP Abnormal Operating Procedure
ARB. Alternate radwaste building
ASME' American Society of Mechanical Engineers
CAL Confirmation of action letter i
CFC Containment Fan Cooler j
CFR Code of Federal Regulations l
CIV containment isolation valve
DC Deficiency card
DRP Division of Reactor Projects
EDG Emergency diesel generator i
Electric Power Research Institute
'
ESF Engineered safety features
ESFAS Engineered safety features actuation system
TSAR Final Safety Analysis Report ;
NUT Holdup tank
I&C Instrumentation and controls
IFI Inspector follovup iten
IST Inservice test
kV Kilovolt
LCO Limiting condition for operation
LER Licensee Event Report
NWO Maintenance work order
NRC Nuclear Regulatory Commission
NRR Nuclear Reactor Regulation
NSCW Nuclear service cooling water
NSSS Nuclear steam supply system
OI Office of Investigations
PM Preventative maintenance
PRB Plant Review Board
psig Pounds per square inch gauge
QA Quality Assurance
RII Region II Office
l REA Request for engineering assistance
RG Regulatory Guide ,
'
SER Safety Evaluation Report
j SI safety injection
i SONOPCO Southern Nuclear Operating Company
- SRM Source range monitor
. SS shift superintendent '
SSS Shift support supervisor
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DRAPT - PREDECISIONAL INFORMATION
APPENDIX 3 '
LIST OF ACRONYMS (continued)
STS Surveillance task sheet
TCP Temporary change to procedure
TS Technical Specification
USS Unit shift superintendent
UV Undervoltage
VEGP Vogtle Electric Generati!.g Plant
VIO Violation
,
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