ML20129F599

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Accepts Offer to Present Evidence in Matter of Alleged Deliberate Provision of Inaccurate & Incomplete Info by Gpc to NRC Re Testing of Emergency Diesel Generators at Facility
ML20129F599
Person / Time
Site: Vogtle Southern Nuclear icon.png
Issue date: 08/23/1992
From: Vorse J
NRC OFFICE OF INVESTIGATIONS (OI)
To: Lavine B
TROUTMANSANDERS (FORMERLY TROUTMAN, SANDERS, LOCKERMA
Shared Package
ML20129F106 List:
References
FOIA-94-208 NUDOCS 9610070002
Download: ML20129F599 (9)


Text

August 23, 1992 Mr. Bryan B. Lavine Attorney at Law Troutman Sanders Nationsbank Plaza, Suite 5200 600 Peachtree Street, N.E.

Atlanta, Georgia 30308-2216

Dear Mr. Lavine:

The purpose of this letter is to formally accept your offer to present evidence, on behalf of your client, Georgia Power Company (GPC), in the matter of the alleged deliberate provision of inaccurate and incomplete information, by GPC to the Nuclear Regulatory Commission (NRC), regarding the testing of the emergency diesel generators at the Vogtle Electric Generating Plant, Unit 1, immediately subsequent to the Vogtle Site Area Emergency of March 20, 1990.

Regarding the NRC personnel to attend you, presentation, in addition to Office of Investigations personnel, it has been requested that representatives of the NRC Office of Enforcement  ;

and Office of General Counsel also be present. I believe that i you would agree that such attendance is appropriate.

Please contact Investigator Larry L. Robinson of my office, at (404) 331-6509, to arrange a mutually agreeable schedule.

Sincerely,  !

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1 James Y. Vorse, Director l Office of Investigations Field Office, Region II i Distribtulon:

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UNITED STATES

!' NUCLEAF, REGULATORY COMMISSION  :

"r e OFFICE OF INVESTIGATIONS FIELD OFFICE, REGION 11 l 4 ..r.

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... titrsdat lapuay 2p, ImM Ga. Power probed by feds  : ,

a 11 _j s e t was undergoing maintenance at Those tapes werelater turned AllegCU l.IC 3DOut Salety Of VOgtie ihe time of the accideni and was over to the NRC. Accordin, io not operable. Mr. Kohn, the tapes are the

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IS 10CUS Of Crinlinal InVCStigat10n During the blackout, um tuu- " linchpin"of the criminalinves- . .

perature of water used to keep tigation. y , ~, " -

By David Beasley Mr.Mosbaugh who specializesin the nuclear fuel from melting Georgia Power spokesman i %~ ,,

stan wmrta whistleblower cases, said a fed. heated from 90 degrees to 136 Tal Wright declined to comment eral grand jury has been con. degrees, the NRC says. on the criminal imystigation. t ,

The U.S. Justice Department vened in Atlanta to consider the Georgia Powerofficials alleg- But in a ste ement,the utility a I is conducting a criminal investi- case. edly told NRC officials that the denied ever attempting to mis-

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getion into allegations that Geor- Joe Whiticy, U.S Attorney generator's mechamcal prob- lead NRC. . .

4 gia Power Co. officials hed to the for the Northern District of lems were quickly corrected.  ;" e ,

But, according to Mr. Mos- And they pomt out that a 14- ,

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Nuclesr Regulatory Commission Georgia, declined to confirm or (NRC) tbout the safety of Plant deny the existence of a grand baugh, the generator continued bor Department Iaw udge administrative g l that Mr. Mos- -

jury investigation as did a to be mechanically unreliable Vogtle near Augusta- b l

The investigation was con- spokesman for Georgia Power. and several components eventu. -

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ally had to be replaced. *that decision is under review t firmed for the first time by the ,s Mr. Mosbaugh, formerly the by the omce of the US. Labor NRC in documents filed recentlY Most serious charge: They lied in the case of Allen L Mosbaugh, third highest ranking manager at Secretary. ,

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a former high-ranking manager The most serious of Mr. Mos- Vogtle, claims in a complaint in a separate action,Mr. Mos-

@[p iA at the nuclear plant,invohed in a baugh's charges is that Georgia filed with the U S. Department of baugh has filed a petition with lergthy whistleblower action Power officials tied to the NRC labor under a law designed to NRC seeking to block transfer of *" ~

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about the reliability of a crucial protect wListleblowers that he the Vogtle license from Georgia og: inst the utility, '

In the document. NRC de- backup generator following a was demoted after complaining Power to a utility subsidiary, clines to comment on Mr. Mos- March 1990 accident at the plant. about safety problems at the Southern Nuclear Operating - - ' ume

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b ugh's allegations because The generator failed after the plant. Company, because of the alleged lie later was fired after Geor- safety violations. ~ .' ~

"these silepations are being pur- regular power supply was "***UG" t

sued by the Department nf Jus- knocked out by a truck that hit a gia Powerlearned that h had se- In documents filed during  ;

tice for possible criminal prose- pole, causing a 36-minute cretly tape-recorded conversa- that proceeding, NRC acknowl- An aNegation that Georgia Power officials tied to the NRC cution." blackout tions with fellow plant em- edges for the first time the exis. about the M?ty of a crucial backup generator following a Michael Kohn, attorney for A se nd backup generator playees. tence of a criminalinvestigation. March 1990 act dent at Plant Vogtle is under irwestigation.

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UNIT 1 /[/ / jPf DIESEL M TOR 18 /

WA DATE TIE COP 90TS 02/24/90 1425 Started for 24 Hour Run 02/25/90 2206 Secured from 24 Hour Run 2336 Started for ESFAS Testi,g 2348 Secured for ESFAS 02/27/90 0312 Started for ESFAS  :

0424 Secured for ESFAS 0605 Started for ESFAS ,

0642 Secured for ESFAS ..

j 03/13/90 1518 Start for thint. Test 0146 Stopped 03/14/99 03/21/90 2149 Failed to start due to insufficient fuel in fuel lines after maintenance.

2156 Failed to Start Again 2202 Started and Governor Vented 2217 Stopped 2259 Started for Overspeed Trip Test 2301 Stopped Manually due to Low Lube Oil Pressure and High 011 Filter DP 2314 Started 2318 Stopped .

03/22/90 0017 Started 0023 Stopped for Maintenance 0426 Started for Testing 0429 Stopped 0714 Locally Started for Maintenance and Engineering Testing 03/22/90 1030 Locally Shutdom i,

03/22/90 1106 Started from CR 1243 Tripped on D/G High Lube Oil Temp.  ;

d 03/23/90 0509 Started for Maintenance Run 1202 Stopped

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. UNIT 1 DIESEL GENE 1tNTUlFIB (CONT'D) i DATE TIE Cop 0ENTS I

I 03/23/90 1730 started for 4 Hour Run  ;

1731 Tripped on Low Jacket Water Pressure / Turbo Lube i

011 Pressure Low i

1744 Started for 4 Hour Run l

' 2222 Stopped 03/24/90 0048 Started for Maf atenan::a 4

0049 "Hi Jacket Water Temp" Alare In, Temp Verified

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to be Noma 1. l

! 0121 Normal Stop J -

03/27/90 1649 Emergency Start Test l

1822 Normal Shutdown i

i 1909 Normal Start 1948 Stopped. Simulated Hi Temp Lube 011 Trip 1951 Started. Simulated LOSP at Engine Panel i

i 1954 Stopped. Simulated Hi Vibration Trip L 1957 Normal Start 1959 Stopped. Simulated Hi Crankcase Pressure Trip 2004 Started. Simulated SI at Engine Panel 2010 Stopped. Simulated to Lube 011 Pressure Trip I 2220 Started. Simulated Bus UY Signal i 2317 Nomal Shutdown ,

l 0403 Startad. Surveillance 14980-1 l' 03/28/90 0537 Normal Shutdown l

! 1350 Start to Perfom Functional Test for WO 1-89-03281 (Lo Lube 011 Pressure Trip Flow Orifices) e 1355 Nomal Shutdown 1356 Started. Simulated UV for Functional on WO

) 1-89-03281 1400 Normal Shutdown hygjg #

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/- 04/01/90 1623 Nomal Start g/ggfy y 1744 Nomal Shutdown h

( Started for Maintenance 04/04/90 1632 1744 Stopped J

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  • UNIT 1 DIESEL GDIE M 18 (CONT'D)

DATE TIE C(300fT5 j 04/05/90 0030 Started. T-ENG-90-17 0035 Stopped 0307 Started. 14980 0509 Stopped d

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b-hM6YA DIESEL TOR 1A 9.

DATE TIIE C089ENTS xa l 02/26/90 1509 Started. 24 Hour Run for ESFAS 02/28/90 0226 Secured from 24 Hour Run 02/28/90 0945 Started for ESFAS Testing j 1210 Secured for ESFAS Testing 1

02/28/90 1700 Started 3 Times in Series During ESFAS Testing 1 02/29/90 0218 Secured for ESFAS Testing )

03/01/90 0128 Started for ESFAS '

03/02/90 0215 Secured for ESFAS 0912 Started for Maintenance 1 1944 Secured for Maintenance J 03/12/90 1306 Started 2137 Stopped 03/13/90 0009 Started 0506 Stopped

03/20/90 0820 LOSF uccurred - Lost "A" RAT - DG1A Tied and 1 Tripped (Several Alarms came in - not noted in the log.)

0841 Auto Started after Sequencer Reset and Tripped on Low Jacket Water Pressure

! 0856 Emergency Break Glass Start Locally to Recover

- from Station Blackout, j 1029 RAT "B" Energized 1040 IBA03 Energized from "B" RAT 1326 Shutdown 2119 Started for Troubleshooting 2206 Shutdown 2223 Started for Trouble nooting 2228 Secured 2233 Started for Troubleshooting 2254 Secured 03/23/90 0254 Started for Maintenance Troubleshooting 0450 Secured 000:m5.

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. UllIT 1 DIESEL EENESTOR 1A .

DATE TIIE CopOENTS 2

03/23/90 1724 Started and Manually Stopped from CR j i

03/29/90 1109 Started. UV Test. Tied to 1AA02 o) 1158 Normal Shutdown 03/30/90 1920 Emergency Start  !

- 2115 Stopped  ;

. 2235 Local Start 2241 Trip Hi Temp Lube 011 2254 Local i i 2300 Trip High Yibration I t

2313 Normal Start ,

l 2316 Stopped. Hi Crank Case Pressure 2328 SI 2334 Low Lube 011 Pressure ,

! 2343 Normal Start 2347 Normal Stop s

2348 Nonnal Start ,

2358 Stop 03/31/90 0012 Normal Start 0024 Ndraal Stop

0016 SI 0019 CR 1827 Start Local 1837 Local Stop 1846 Local Start 1847 Stop i

1856 Local Start 1857 Local Stop 1904 Local Start 1906 Local Stop 1921 Local Start '

1922 Local Stop Onn.'t.%

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DDb UNIT 1 DIESEL EEREBToa 1A DATE TIfE COBOENTS 03/31/90 1955 Local Start Local Stop 2012 2254 Started. UV Test, Tied to 1AA02 .

2320 Normal Shutdown 04/01/90- 0423 Started. Surveillance 14980-1 0556 Nonnal Shutdown 04/06/90 1345 Start. T-ENG-90-16 1346 Stop 1404 Start. T-ENG-90-16 1405 Stop

< 1419- Start. T-ENG-90-16 1430 Stop l 2347 Start. T-ENG-90-11 '

04/07/90 0213 Stop 4

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WASHINGTON, D C. 20065 Dir 4

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%. July 6, 1993 ._._ Ad _ _ _ _ __

_FOIA enain"*" __Suppon __

File . /

) Copies to: A L -

l The Honorable Joseph I. Lieberman, Chairman Subcomittee on Clean Air and Nuclear "99ulation a Coenittee on Environment and Public Works United States Senate

Washington, D.C. 20510

Dear Mr. Chairman:

4 l Pursuant to conversations with your staff. it is our understanding that you are planning to hold a hearing on the Nuclear Regulatory Comnission's handling of whistleblowers in the nuclear industry and that you may call Mr. Allen

Mosbaugh and the Georgia Power Company to testify regarding Mr. Mosbaugh's experiences as a whistleblower prior to and after the site area emergency of j March 20, 1990, at the Vogtle nuclear power plant.

On June 24, 1993, the NRC Atomic Safety and Licensing Board in the ongoing

Georgia Power Company license amendment proceeding determined that six tape recordings made by Mr. Mosbaugh, which are copies of portions of a larger number of tapes, should be released to Georgia Power Company in c',covery. We understano that these six tapes, which by agreement among the neties were to
be re%ased on July 2,1993, were previously made available to the Subcomottee by Mr. Mosbaugh's attorney.

We understand that the Subcommittee does not intend to seek or compel the public disclosure of material compiled by the NRC's investigatory staff that

is not already in the public record, or seek public disclosure of substantive

. conclusions that the investigators may have reached on matters under j investigation.

The Director of the Office of Investigations has concluded that public discussion by the Subcommittee of information relating to Mr. Mosbemoh's l allegations with either Mr. Mosbaugh or the Georgia Power Company wi'l not ,

i adversely affect any current matter under investigation by his .

However, neither the Commission nor its staff will be in a pos s
either the NRC investigation or any potential effect of the inves possible enforcement actions or on the angoing licensing proceeding.

Sincerely, l

. J l

Kenneth C. Rogers Acting Chaiman ,.

cc: Senator Alan K. Simpson

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i ELECTRICAL POWER SYSTEMS f SURVEILLANCE REQUIREMENTS (Continued) l At least ones per 10 years or after any modifications which could

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affect diesel generator interdependence by starting both diese h i

generators simultaneously, during shutdown, a 7

equal to (103 seconds; and

g. At least once per 10 years bye ,

1)

Draining each fuel oil storage tank, removing the accumulate sediment and cleaning the tank using a sodium hypochlorite solution, and Performing a pressure testsubsection of thoseNDportionsof the ASME of the diesel fu

2) oil system designed to Section III, 5 of the systes design Code at a test pressure equal to 110 pressure. (

l ator failures, valid or nonvalid, shall6.F.2 l 408.1.1.3 Ak oo be reported to W_rti - All diesel genere within 30 days.

id 1.108, Revi Commissio

tion recommended in Regulatory Position C.3.b t shall be of Regulatory lt sion 1 August 1977.a per nuclear unit basis is greater than or.. equal to supplemented to include the additional i Position C.3 b of Regulatory Guide 1.108, Revision 1, August 1977 information recommen

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