ML20129F418
| ML20129F418 | |
| Person / Time | |
|---|---|
| Site: | Vogtle |
| Issue date: | 07/23/1991 |
| From: | Reyes L NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| To: | Vandenburgh C Office of Nuclear Reactor Regulation |
| Shared Package | |
| ML20129F106 | List:
|
| References | |
| FOIA-94-208 NUDOCS 9610040144 | |
| Download: ML20129F418 (56) | |
See also: IR 05000424/1990019
Text
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UNITED STATES
'o
NUCLEAR REGULATCRY COMMISSION
.
[
CE! ION 11
.
,
y
,P
101 MARIETTA STREET, N.W.
s
ATLANTA, GEOR0dA 30323
,
'+,.....
JUL 2 31991
MEMORANN N F0P,
Chris A. VanDenburgh, Chief, Reactive Inspection Section 2
Vendor Inspection Branch
Division of Reactor Inspections and Safeguards
FROM:
Luis A. Reyes, Director
e
Division of Reactor Projects
SUBJECT:
V0GTLE SPECIAL TEAM INSPECTION - ALLEGATION FOLLOWUP TEAM
DRAFT INSPECTION REPORT (INSPECTION REPORT NOS. 50-424/90-XX
AND50-425/90-XX)
This memorandum refers to the special inspection conducted on August 6
through 17, 1990, at the Vogtle Electric Generating Plant (VEGP).
This
inspection involved a review of several allegations regarding the safe
operation of VEGP and the review of operational activities generally related
'
to the allegations. As discussed in the inspection plan, the inspection was
performed by two separate teams--an operational followup and an allegation
,
followup team.
As decided in a meeting held in Nuclear Regulatory Commission (NRC) head-
quarters on September 26, 1990, the allegation followup team's findings and
conclusions was not included in Inspection Report 50-424/90-19;
50-425/90-19. This information was to be withheld pending the completion of
an Office of Investigation review of the allegations and the inspection
team's conclusions. On January 11, 1991, Inspection Report 50-424,425/90-19
was issued which included the operational followup team findings.
The
remaining issues from the allegation followup team were then left in
Inspection Report 90-XX, pending the completion of Ois' review of the
allegations.
'
On July 9,1991, a meeting was held in Region II, with members of Region
II-DRP, 01, and NRR-PD3-2 and Regional management.
It was determined to
j
issue the remainder of the 50-424,425/90-19 report, except for the following
i
,
issues: 1) 12.3 Missed Containment Isolation Valve Surveillance; 2) 12.4
-
Mode Change With Inoperable Source Range Monitor Nuclear Instrument; 3) 1
2.7 Reliability of Emergency Diesel Generators and their corresponding parts
to the Notice of Violations.
This memorandum forwards a marked up copy of Inspection Report 50-424,
425!90-19, Supplement 1, which documents the inspection team's review and
conclusions regarding the allegations as of the time of the inspection exit
meeting on August 17, 1990
The report has already been reviewed by the
.
Office of Investigation in Region II for information that clight compromise
'
their on going investigations.
The information that was considered
pertinent to these investigations will not be included in the issued report.
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9610040144 960827
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COLAPIN94-200
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Chris A. VanDenburgh
2
JUL 2 31991
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If you have any questions concerning this issue, please contact P. Skinner
!
at Ext.16299 or S. Vias at Ext.15350.
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Luis A. R
Enclosures
~1.
Draft Notice of Violation
i
2.
Draft -Inspection Report
'
50-424,425/90-19 Supplement I
cc w/encis:
!
L. Robinson 01.
i
D. Hood, NRR, PD3-2~
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6. Jul
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ioi maasts ta sie<tti.
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anc.mA.etonc A 3o323
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Docket Nos. 50-424 and 50-425
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License Nos. NPF-68 and NPF-81
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Georgia Power Company
ATTN:
Nr. W. G. Hairston, III
i
Senior Vice President -
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Nuclear operations
q
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P.O. Box 1295
y
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)
Birmingham, AL 35201
Gentlemen:
SUBJECT:
VOGTLE SPECIAL TEAM INSPECTION AND NOTICE OF VIDIATION
1
(NRC
INSPECTION
REPORT
NOS.
50-424/90-19
AND
3
50-425/90-1gg SuppleAw
This refers to the
inspection conducted by an NRC Special p
!
Inspection Team on August 6 through 17, 1990.Jr Tne inspem. ion .Ag'
i
j
included a
review of activities authorized for your Vogtle
3
i
facility.
At the conclusion of the inspection, thePffindings were
}[
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discussed with those members of your staff identified in the
j
enclosed inspection report.
i
Areas examined during the inspection are identified in the report.
!
Within
these
areas,
the
inspection
consisted
of
selective
examinations of procedures and representative records, interviews
j.
with personnel, and observation of activities in progress.
Based on the results of this inspection, certain of your activities
.
.
appeared to be in violation of NRC requirements, as specified in
j
the enclosed Notice of Violation (Notice).
i
-1^3 *hatthe inspection concluded that the facility was opera
_
a safe mann..- Q dance with the requirements
perating
l
license, we are conc =..:f
that there
e
veral operational
policies and programs whers we
___ -
laantified. As part of
your response to the
ons identified n
sed Notice,
,
you are a
sted to address each of the weaknesses
___A
l
ion summary.
!
!
You are required to respond to this letter and Notice and should
,
follow the instructions specified in the enclosed Notice when
preparing your response to the violations.
In your response, you
1
l
should document the specific actions taken and any additional
i
actions you plan to prevent recurrence.
After reviewing your
response to this Notice, including your proposed corrective actions
'
and the results of future inspections, the NRC will determine
whether further NRC enforcement action is necessary to ensure
compliance with NRC regulatory requirements.
-
.
Q.4 4t g
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coorgio Pov3r CcIpany
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you should respond to each of the o
a
4
esses are
E d!*ionally,
(The
weaknessesMfied within the report.
ary.)
The response
specifically annotated-in .the InspectioMhe s3gnificance of the weaknesses
.
should address your analysis at these operat
tices do not
,
and your actions toof non-compliance or reduce the marg n
7:'ev^
evolve int
p ant.
In accordance with section 2.790 of the NRC's " Rules of Practice,"
.'
a copy of this letter and its enclosures will be placed in the NRC
Public Document Room.
r
The responses directed by this letter and the enclosed
and Budget as required by the Paperwork Reduction Act of 1980,
Pub. L. No. 96. 511.
Should you have any questions concerning this letter, please
contact us.
4
sincerely,
0
>
i
ne
r
f
-
>' Regional Administrator
<
Region II
,
.
l
Enclosures:
1.
Inspection Report 50-424/90-191
2.
50-425/90-19 % (pl* * d 1
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LIMITED DISTRIBUTION - Not For Public Ralesco
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DRAFT - PREDECISIONAL INFORMATION
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May 9,
1991
.
.
,,
MEMO
DUM FOR:
Luis A. Reyes, Director
g:~ y
.i
Division of Reactor Projects
fq ',* :
~
-
Region II
.6.'N ', ' '
NY '- " '-4'.:..T + '-
FROM:
Chris A. VanDenburgh, Chief
.1
Reactive Inspection Section - 2
[5EF.('-j ,y..
Vendor Inspection Branch
Division of Reactor Inspection
and
i
'
Safeguards
SUIL7ECT:
VOGTLE
ECIAL TEAM INSPECTION - ALLEG TION FOLLOWUP TEAM
DRAFT
SPECTION
REPORT
(INSPE
ION
REPORT
NOS.
!
50-424/90
x AND 50-425/90-xx)
l
This memorandum refer
to the special
spection conducted on
August 6 through 17, 19
, at the Vogtle
lectric Generating Plant
.
(VEGP).
This inspection nvolved a rev ew of several allegations
regarding the safe operati
of VEGP a d the review of operational
activities generally relate to the
legations.
As discussed in
i
the inspection plan, the ins
ction was performed by two separate
teams--an operational followup nd n allegation followup team. At
the conclusion of the inspect
all of the inspection team's
,
,
conclusions with respect to the
erations and allegation followup
were discussed with the me
s
GP's staff identified in the
enclosed draft inspection re rt.
I
As decided in a meeting hel in Nuclea
egulatory Commission (NRC)
headquarters on September 26, 1990, the
llegation followup team's
findings and conclusio
have not bee
included in Inspection
Report 424/90-19; 50-4 /90-19. This info
ation has been withheld
pending the completi
of an office of Inve
igation review of the
allegations and the
spection team's conclus
ns. This memorandum
,
forwards a draft
spection report (50-424/
-xx; 50-425/90-xx)
'
s
which documents
e inspection team's revie
and conclusions
regarding the a
egations as of the time of th
inspection exit
'
meeting on Au
t 17, 1990.
The areas e amined during the inspection are iden
fled in the
.
-
inspection eport. As discussed in Inspection Report
-424/90-19;
50-425/90
9, the inspection team concluded that the f
ility was
safely
rated.
However, the inspection identifie
several
'
,
i
instan
s in which the VEGP was not operated in accordance
ith the
,
inten
of
the Technical
Specifications.
In
additio
the
insp ction
identified
several
potential
weaknesses
i
the
'
fa
lities' operational r licies and practicc..
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DRAFT - PREDECISIONAL INFORMATION
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Lui
A. Reyes
-2-
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The ins'pection team's review of the allegations identified severa
additio 1 weaknesses in these operational policies and practice .
These ar
identified in the inspection summary of the enci
ed
,
'
draft insp ction report.
activities app,esults of this inspection of the allegations,
Based on the t
artain
eared to be in violation of NRC require
nts, as
specified in t e enclosed draft Notice of Violation (Notice).
These violations re important because they indicate (
a failure
administrative proc,equirements of the Technical Speci
cations and
to implement the r
9 ures, and (2) the failure to pr vide accurate
d
-
information to the
.
As part of the response to the violations /dentified in the
~
enclosed notice, VEGP should also be requeste
to address each of
'
the concerns listed in t e inspection summa
.
t
Enclosures:
1.
Draft Notice of Violation
2.
Draft Inspection Report 50-434/90-xx; 50-425/90-xx
/
cc:
BKGrimes
EWBrach
.
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LINITED DISTRIBUTION - Not For Public Release
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LIMITED DISTRIBUTION - Not For Public RalGG00
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DRAFT - PREDECISIONAL INFORMATICN
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NRR/DRIS
RII/DRP
RII/DRP
RII/DRP
JWilcox*
RAlello*
RStarkey*
MBranch*
9/ /90
8/31/9
8/31/90
8/31/90
I
RII/DRP
RII
RS
NRR/DLPQ
RJI/DRS
I4arner*
MThomas*
NHuneauller*
ylore
9/27/90
/31/90
8/31/90
8/ 1/90
i
RII/DRP
NRR/DRIS
i
RCarroll*
CVanDenburgh
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8/31/90
9/ /90
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- Se previous concurrences
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LIMITED DISTRIBUTION - Not For Public R31easo
DRAFT - PREDECISIONAL INFORMATION
ENCLOSURE 1
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NOTICE OF VIOIATION
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Georgia Power Company
Docket Nos. 50-424 and 50-425
Vogtle Electric Generating Plant
License Nos. NPF-68 and NPF-81
Units 1 and 2
3
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During an NRC inspection conducted on August 6 through 17, 1990,
,
violations of NRC requirements were identified.
In accordance with
the " General Statement of Policy and Procedure for NRC Enforcement
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Actions," 10 CFR Part 2,
Appendix C (1990), the violations are
!
listed below.
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A.
10 CFR Part 50.9, " Completeness and Accuracy of Information,"
requires that info mation provided to the NRC by a licensee
"
shall be complete and accurate in all material respects.
I
Contrary to the above,
the licensee provided g curate
information
to
the
inspection
team
on 4heee
separate
,
1
occasions. Although the information was provided in unsworn,
1
oral statements, the information provided was significant to
the licensing process.
The information was provided by
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licensed operators, supervisors and management concerning
i
information which was within their specific responsibilities.
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The d4ve examples were as follows.
(50-424/90-eese-95; 50-
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90-eas-99)
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IV'2-
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1.
Containment
Isolation
Valves:
During
a
Unit
2
,
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surveillance procedure, the unit shift supervisor (USS)
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stated, and the operations manager later confirmed, that
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the containment isolation valves for the hydrogen monitor
system were allowed to be opened without entering the
3
3
limiting
condition
for
operation
(Ico)
action
requirements for Technical specification (Ts) 3.6.3
because the valves
received an automatic
isolation
.3
signal. The inspection identified that these containment
]
isolation valves were remotely-operated, manual valves
without automatic isolation signals.
(Discussed in
Section 2.2.1.1 of Inspection Report 50-424/90-19; 50-
425/90-19)
2.
Snubber Reduction:
The operations manager stated that,
4
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after the second Unit i refueling outage (1R2), the
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modifications to tt:e snubbers were done in conjunction
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personnel Accountabiliev: The operations manager stated that
the shift superintendents (SSs) reported directly to the
operations manager and that he personally prepared their
performance appraisals.
The inspection identified that the
sss reported to the unit superintendent (Us), and that the US
1
personally prepared the performance appraisals of the Sss.
j
(Discussed ;,n section 2.Af of this inspection report)
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Ts 3. 0. 3 Actions:
The unit superintendent indicated that
there were no Operations
Department actions which were
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,2
anticipated or required within the first three hours of
'
entering the action statement of TS 3.0.3.
The inspection
identified that the VEGP management policy and stated practice
required preparations
for a
power
reduction,
including
,
8
informing
the
load
dispatcher within
the
first
hour.
(Discussed in section 2.1.1.3 of Inspection Report 50-424/90-
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19; 50-425/90-19)
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with preplanned system outages which were required for
i
other preventive or corrective maintenance or testing.
The
inspection
identified that
few of the snubber
<
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modifications were done jointly with pre-planned system
i
outages.
(Discussed in Section 2.1.1.4 of Inspection
j
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Report 50-424/90-19; 50-425/90-19)
'
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Diesel-Generater (w)
- =14mhl11tyr
vrco
j
E== v.nq
.ncorrectly counted the number of starts and failurgot
,
1
t
DGs and incorrectly represented the EDG re ability
i
in a
on II presentation on April 9, 199
Although
t
I
the presen
ion was not 'ntended to repr sent a specific
,
number
of
su
ssful
valid
test
s specified
in
Regulatory Guide (
1.108 and T
. 8.1.1.2a, but rather
,
i
to describe the EDG ma
nan
test program and the EDG
,
reliability status, the
was not informed of the
i
incorrect information
il th
C asked for it during
j
the inspection.
he confirmat
of action
(CAL)
i
response and L
nsee Event Report (LER
-006 were also
,
incorrect A cause they were based on t
EDG start
l
inform fon that was compiled for the VEGP pre
ation
I
j
in
e Region II Office.
(Discussed in Section 2.
f
g[
s inspection report)
I
This is a Severity M vel IV violation (Supplement VII).
2
l
B.
Technical Specification 6.7.1.a
requires
that
written
j
procedures be established or implemented for those activities
delineated in Appendix A of Regulatory Guide 1.33, Revision 2,
'
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February 1978.
l
Contrary to the above, two examples were identified in which
the licensee failed to establish or implement the procedures
for these required activities as follows:
(50-424/90-ac'M? :
19- G
50-425/90-asu-49)
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19 - 6
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1.
Administrative Procedure 00150-C, " Deficiency Control,"
i-
states that a deficiency card must be written if the
deficiency involves safety-related components which are
i
to
be
dispositioned
"use-as-is/ repair,"
or
other
conditions
involving safety-related components which
require engineering support or other technical assistance
-
to determine if the component is deficient.
d
on August 17, 1990, the NRC identified that a deficiency
card was not written on re'idual heat removal (RHR) pump
f1B (a safety-related component) to document the pump's
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degraded conditions which were dispositioned "use-as-is".
(Discussed in Section 2.2 of this inspection report)
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2.
Administrative Procedure 00100-C,
" Quality Assurance
Records Administration," Paragraph
4.1.1.8,
specifies
that
quality
assurance
(QA)
records
will
exh! bit
necessary and appropriate signatures or initials and
[
dates.
.
On August 17, 1990, the NRC identified that the Unit
i
Superintendent incorrectly initialed, dated, and signed
i
a QA record which voided Temporary Change Procedure (TCP)
1802-C-7-90-1 to Abnormal Operating Procedure 18028-C,
" Loss of Instrument Air," with the date of June 12, 1990,
i
in lieu of the actual date (June 15, 1990) on which the
document was signed.
(Discussed in Section Jdf of this
'
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inspection report)
g.1b
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{
This is a Severity Level IV violation (Supplement I).
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C=
re. ::, w=n= :. cra.r4
--cI,
corr.cu=
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Action," requires measures to be established to ensure tha [
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onditions adverse to quality are promptly identified f d
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c
rected.
In the case of significant conditions adve Ne to
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qua
, the measures are required to ensure that theguse of
i
the co
tion is determined and corrective action Jd taken to
i
preclude
tition.
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Contrary to th
ve, two examples were identified in which
,
preclude repetitl'o/aplement
to determine and
adequate
the licensee fa
d
n as follows:
(50-
corrective actions
l
424/90 .ans- et)
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14 - 14
/
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1.
On August 17,1900, theWC4etermined that the licensee
"
did not identify the foitat and normal use of the 14:0
.
status sheet as one oJA.he causes of the event described
j
in Licensee Event Report (LER) '90,-004, " Failure To comply
With Technical Specification 3.0N< occurs on Entry Into
Mode 6"; therefore, corrective action was not taken to
,
preclude repet'ition of the failure to review Ico-required
actions orAremarks which may be on the back side of the
i
LCo status sheet.
(Discussed in Section '2.4
of this
,
inspect' ion report)
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2.
(chnical Specifications 4.8.1.1.3 and 6.8.2 require hat
all valid or non-valid EDG failures be reported to th
NRC in a special report within 30 days.
In addition,
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DRAFT - PREDECISIONAL INFORMATION
'
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Operations Procedure 55038-C, " Diesel Start Log," Section
. 0, requires that all EDG failures shall be re or(ed to
'
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t
RC in a special report.
!
On Augu
17,
1990,
the
NRC
ideptified
that the
j
corrective a
ions taken in response 4o a previous notice
inadequate./ Inspection Report 50-
'
of violation
e
.
424/s7-57 (dated
aber S A987) previously identified
j
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a violation of Tech ' al Specification
4.8.1.1.3,
in
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that, all EDG failuresmo
not reported to the NRC in a
special report. During a re
w of the start records for
i
EDG f1B duringA:he period of
h 21 through June 14,
i
1990, the NBC' identified that EDG
lures had occurred
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which were'not submitted to the NRC in
special report.
In a difion, the NRC identified that Opera
ns Procedure
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8-C provided inadequate guidance to i
tify and
classify EDG failures.
(Discussed in Section 2.
this
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inspection report)
This is a Severity I4 vel IV violation (Supplement I).
!
Pursuant to the provisions of 10 CFR 2.201, Georgia Power Company
is hereby required to submit a written statement or explanation to
i
the U.S. Nuclear Regulatory Commission, ATTN:
Document Control
,
Desk,
20555,
with a copy to the Regional
Administrator, Region II, and, if applicable, a copy to the NRC
Resident Inspector within 30 days of the date of the letter
i
transmitting this Notice Of Viel: tic . (;5tia) . This reply should
be clearly marked as a " Reply to a Notice of Violation" and should
include for each violation:
(1) the reason for the violation, or,
if contested, the basis for disputing the violation,
(2) the
corrective steps that have been taken and the results achieved, (3)
the corrective steps
that
will
be taken to avoid
further
violations, and (4) the date when full compliance will be achieved.
If an adequate reply is not received within the time specified in
this Notice, an order may be issued to show cause why the license
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should not be modified, suspended, or revoked, or why such other
action as may be proper should not be taken.
Where good cause is
shown, consideration will be given to extending the response time.
,
FOR THE NUCLEAR REGULATORY COMMISSION
l
Stuart D. Ebneter
Regional Administrator
Region II
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Dated at Atlanta, Georgia
this
day of
199p
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50-424/90-N and 50-425/90-N , $u f pleMe aN I
Report No.:
Licensce:
Georgia Power company
P.O. Box 1295
Birmingham, AL 35201
.
Docket Nos.: 50-424 and 50-425
License Nos.: NPF-68 and NPF-81
Facility Name:
Vogtle Electric Generating Plant, Units 1 and 2
i
Inspection Conducted:
August 6-17, 1990
1
Team Members:
Ron Aiello - Resident Inspector, Vogtle
Morris Branch - Senior Resident Inspector, Watts Barr
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Robert E. Carroll, Jr. - Project Engineer, DRP, Region II
Larry Garner - Senior Resident Inspector, Robinson
Neal K. Nuneauller - Licensing Examiner, NRR
Larry L. Robinson - Investigator, 01, Region II
Robert D. Starkey - Resident Inspector, Vogtle
Craig T. Tate - Investigator, 01, Region II
Peter A. Taylor - Reactor Inspector, DRS, Region II
McKenzie Thomas - Reactor Inspector, DRS, Region II
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John D. Wilcox, Jr. - Operations Engineer, NRR
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Team Leader:,.
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" Chfis E Va'nDenburgh, SectTon C'hief
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Division of Reactor Inspections and Safeguards
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Office of Nuclear Reactor Regulation
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Appeeved by:
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a s . ten m< =~e m. --3 =t a -
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suf W f
90,
TABLE OF CONTENTS
g
INSPECTION SUMMARY........................................
-t"
T'
1.0
INS PECTION OBJ ECTIVES . . . . . . . . . . . . . . . . . . . . . . . . .
.....
2.0
ALLEGATION FOLLOWUP..................................
Ar
2.1
Improper Installation of FAVA System............
9-
2.2
Operability of Residual Heat Removal Pump.......
41-
2.3
Mi.e.d -Ce..teinsent Isc1; tion '!;1v; Ourveillance.
10
2.4
Msde Cheng; "'ith In:perable Source Rang?
3 -Moni te r Ne:l e r ! n t re :n t . . . . . . . . . . . . . . . . . . . . . .
10-
2 .JF Backdating o f Signatures. . . . . . . . . . . . . . . . . . . . . . . . jkP
2.sr Reportability of Previous Engineered Safety
Y Features Actuation System Load Sequencer
24'
Outages.........................................
3.'
Reliability cf Esergency Olcsci Cenereters. . . . . .
2-
2.,r
Air Quality of Emergency Diesel Generator
6 Starting Air System.............................
34F
b eportability of Previous System Outages........
25'
R
2.F
'2..'7 .240 Intimidation of Plant Review Board Members. . . . . .
33-
2 b L kT Personnel Accountability........................
,3&-
3.0
EXIT INTERVIEWS......................................
)4P
APPENDIX 1 - LIST OF TRANSCRIBED INTERVIEWS. . . . . . . . . . . . . . . JFr
APPENDIX 2 - PERSONS CONTACT 2D. . . . . . . . . . . . . . . . . . . . . . . . . . . .
J1r
APPENDIX 3 - LIST OF ACRONYMS . . . . . . . . . . . . . . . . . . . . . . . . . . . . .
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DRAFT - PREDECISIONAL INFORMATION
INSPECTION SUMMARY
Recent activities which have occurred at the Vogtle Electric
Generating Plant (VEGP) have raised concerns within the Nuclear
Regulatory Commission (NRC) as to the ability and the deterinination
of the licensee to operate the facility in a safe and conservative
manner. To address this concern, the NRC performed a special team
inspection to deter 1mine if the licensee operates the facility in
accordance with approved procedures and within the requirements and
,
intent of the facility's operating license.
In addition to the
occurrence of specific events, NRC concerns regarding the safe
operation of the facility were heightened with the receipt of
several allegations relating to operational activities at VEGP.
The aggregation of the facts and circumstances associated with the
operational events and the allegations was viewed as a possible
indicator of a non-conservative attitude on the part of the
facility's operating staff which warranted the immediate initiation
I
of special inspection activities.
Specifically, the inspection objectives were to:
1)
Assess the operational philosophy, policy, procedures and
practices of the f acility's operating staff and management
regarding operational safety.
'
2)
Determine the technical validity and safety significance of
{
- d cf the allegations and their impact on the safe and
conservative operation of the facility.
These inspection objectives were accomplished by the use of two
inspection teams--an operations followup team and an allegations
followup team.
The offorts of these two inspection teams were
closely coordinated;
however,
they independently pursued the
objectives outlined above.
The operations followup team monitored control room activities on
a 24-hour basis
in order to:
(1)
evaluate the operational
philosophy, policies, procedures, and practices of the operating
.
staff and management and (2) determine if the plant was being
i
operated in a safe and conservative manner in accordance with the
l
facilities' operating license.
!
The allegations followup team verified the technical validity and
safety significance of each ef the allegations.
In addition, with
k
the assistance of the OI staff, this team interviewed * members of
the plant
staff
in order to
determine
(1)
their personal
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involvement and knowledge of the specific allegations and (2) their
practice and understanding of the station operational policies.
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These-interviews were transcribed. Although an OI investigator was
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assigned to the inspection team to assist during the transcribed
1
interviews, this inspection was not an investigation into th
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intent of the alleaed violations. Nu muesrep.a5 **t
w (:iewen. e<mo not iunst.
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The inspection substantiated the occurrence of the specific events
described in the allegations.
These events resulted i
t
q
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examples o
v, lations of regulatory requirements (50-424/90-
D
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50-425/90-
)2' "" G/^; .. ;^ ; and two of the events were
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previously identified as non-cited violations (50-424/90-10-03 and
50-425/90-01-01).
- : : , the ine;rrtier did net rubettntirt
d
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-th:t th: : ::t: :' vielstien
vere-perfe n f rith the full-
L,wledge of 'J::Or ::n:; ::nt.
Sie cerclerier See herM rper :
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' ;vice Of the lic:::ee's recorde
^^d
the Svern testisery ef the
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pe;ple inv;17;d in th: ev::t;.
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inspection
also
identified
that
on
several
oc
s
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respons
agers and supervisors verbally su
naccurate
information to t e '
tion team durin
spection. Although
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the inspection team was
a out the accuracy of the
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information provided
an did n
a basis to conclude or
suspect th
examples were the result o
ss disregard
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,
atory requirements or individual wrongdoing.
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Ioom m.' ' b observations and conclusions of the inspection tem #g::o )
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50-424/90-19; 50-425/90-1C In ,)#-
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are detailed in Inspection Report
addition, the bases for these previous conclusions are summarized
below.
4
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Doerational Policies and Practices
3
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NRC Inspection Report 50-424/90-19; 50-425/90-19 identified several
examples in which the licensee's operational policies and practices
'
had the potential to adversely affect the operation of the
i
facility.
llegation followup team's review of the allegations
identifiedn
additional examples in which the licensee's l
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operational policies and practices had the potential to adversely
affect the safe operation of the facility 1
"^r err;1:-
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1)
The licensee's method of conducting Plant Review Board (PRB)
meetings had the potential for adversely affecting open
,
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discussions among the PRB members.
This concern was based on
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an example in which a PRB voting member felt intimidated and
feared retribution during a PRB meeting because of the
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presence of the general manager and the absence of dissenting
opinions in the PRB meeting minutes.
Continued licensee
action is necessary to ensure that PRB members freely and
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openly express their technical opinions and safety concerns.
(Section.2AC)
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2)
The
licensee's
practice
of
signing
and dating
quality
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assurance records was controlled by administrative procedures;
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however, there was a confirmed exasple in which a signature
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was backdated to reflect the actual date of performance.
The
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backdating
of
1802-C-7-90-1
was
verified
and
was
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identified as Violation 50-424/90-
~6;
50-4 25/90-aus-et .
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(Section 24)
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3)
The licensee' practice of not initiating a deficiency card
(DC)
during
troubleshooting
activities
involving
the
questioned operability of the residual heat removal (RHR) pump
prevented a documented engineering evaluation for either the
nuclear service cooling water (NSCW) outlet leak or the
excessive vibration on the RHR motor.
The
fal' lure to
,
implesent this administrative procedure was identified as
.4
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Violation 50-4 2 4/90 .xas-@2.
(Section 2.2)
si-4
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"; 11::ncer '
- the ef 59*= 4 = 4 a0 ==d eaaWal l i a; en,a 4 == af
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completed surveillance procedures was not controlled
y
,
inistrative procedures.
Based on the confusio
hich
i
resu
d
in the missed
curveillance of the
tainment
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isolatio
alves and a review of this methodo
additional
atter. tion
acessary to ensure that thg
procedures are
3
2
appropriately c ntrolled and used.
(Sect' ion 2.3)
!
,9)
The licensee's math
to
denti
tive and informational
limiting condition for oper
.ns (Iros) on LCO status sheets
allowed continuation o
he ~I40 required ac.tions on the
reverse side of the
rm.
This me
in conjunction with
,
the operator's c
reed practice of re
wing only the front
'
side of the
status sheets, was one of
oot causes for
l
a non-ci
violation (50-424/90-10-03) conc
ng a mode
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cha
ich occurred with inoperable source ra
uclear
i
ruments.
The failure to identify this additiona
oot
... la.ni.iii.4 es Vicletie.. 50 4 ?/00 ::
^3.
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The licensee's method of appraising the performance of the
licensed operators resulted in a potential disincentive for
identifying items which may result in LERs or violations,
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(Section 2 44)
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DRAFT - PREDECISIONAL INFORMATION
Accuraev of Information
The inspection concluded that during the inspection inaccurate
information was received on several occasions, from responsible
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managers and operators on topp:s well within the scope of * a ir
specific responsibility. In 4Manstances the initial infor Cisn (
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supplied was clearly incorrect or inadequately researchef
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inspection team concluded that in each of these example:
th t
licensee officials provided inaccurate, unsworn, oral stat cent s
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concerning information which concerned topics well within ts.24r
responsibilities,
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In
the 4ir;t
th:::
cases,
the
inaccurate
information
was
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significant to the inspection process.
Specifically, (1) if the
i
containment isolation valves received an automatic closure signalthe v
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if the snubber modifications had been performed in conjunction with
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other preplanned preventive and corrective maintenance, then the
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voluntary entries into LCO 3.7.8 would not have been required, end- I
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p) ii the-WRC-was.. accurately informed .cf.-the-aumber of p
51:::
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and i.ilorse ;' - th: Ere:gency Diesel Cenerator-No.
15 ehich
uwwuu.a dosinii ts d10 h:: ting, ther additiert! tecting rey hr :
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,.... . .,,. is .4- pries to - th: rele::: .. .... ....... _..... .. ::tden
1etten The inspection team concluded that the failure to provide
accurate information was a violation of the requirements of 10 CFR 50.9 concerning accuracy and completeness of information.
The
inspection identified Violation 50-424/90-
- 50-425/90-Jsw-99 in j
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this area and ncted the following examples:
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1)
containment Isolation valves:
During a Unit 1 surveillance
procedure, the unit shif t supervisor (USS) stated, and the
operations manager later confirmed, that the containment
,
.
isolation valves for the hydrogen monitor system were allowed
to be opened without entering the 140 action requirements for
i
TS 3.6.3 because the talves received an automatic isolation
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signal.
The inspection identified that these containment
isolation valves were remotely-operated, manual valves without
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auta.tatic isolation signals.
(Discussed in Section 2.2.1.1 of
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Inspect Dn Report 50-424/90-19; 50-425/90-19)
2)
Snubber Reduction:
The operations manager stated that, after
Unit 1 refueling outage IR2, the modifications to the snubbers
were done in conjunction with preplanned system outages which
i
were required for other preventive or corrective maintenance
or testing. The inspection identified that few of the snubber
modifications were done jointly with pre-planned system
i
' outages.
(Discussed in Section 2.1.1.4 of Inspection Report
50-424/90-19; 50-425/90-19)
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Emeraenev Diesel cenerator Reliability: The licensee's met
researching
information
for
Region
II
prese
ion
{
ng the reliability of the emergency diesel ,
erators
conc
(EDGs) v
nadequate in that there was a 1
of specific
l
. guidance conc
ng the EDG information d
red coupled with
I
inadequate resear
the EDG starti
story.
This method
resulted in providing
omplete
therefore, inaccurate
i
,
info mation to the NRC.
inn
lon, the licensee's response
to the NRC's confi nation
ac
letter (CAL) was based on
,
i
this same inadequate
earch.
In
tion, the subsequent
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Licensee ' Event
rt (LER)90-006 was
so
inadequately
!
researched.
a result of this method of inv
ation, the
i
NRC was
r informed of the correct operability a
until
j
this
pection.
(Discussed in section 2.7 of this inspe
n
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ort)
34t
Personnel Accountability: Theoperationsmanagerstatedthatl
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the shift superintendents (sss) reported directly to the
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operations manager and that he personally prepared their
i
performance appraisals.
The inspection identified that the
SSs reported to the unit superintendent (US), and that the US
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personally prepared the performance appraisals of the SSs.
!
(Discussed in Section 3 A 1 of this inspection report)
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4pf
ts 3. 0. 3 Actione:
The unit superintendent indicated that
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there were no operations Department actions which were
i
anticipated or required within the first three hours of
i
entering the action statement of TS 3.0.3.
The inspection
!
identified that the VEGP management policy and stated practice
!
required preparations
for a power reduction,
including
i
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informing
the
load
dispatcher within
the
first
hour.
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(Discussed in Section 2.1.1.3 of Inspectica Report 50-424/90-
its 50-425/90-19)
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In summary, the inspection identified these violations and two\\
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inspector followup items. The violations involved: (1) a violation
i
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of 10 CFR 50.9 in that responsible licensee officials provided
inaccurate information to the NRC during the inspectionf4(2) a
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violation of TS 6.7.1.a in that, two examples were identified of
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the licensee failing to }mplement actions in accordance with
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administrative procedures /, M _f')
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W '. 2, 0: iter!:: "Y!, in th:t, tt:0 ::: ;1 : ::: id:nti f'<ed-of
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th; li;;;;;; i pi::: ting in:d:ptt: ::rr :tiv: ::ti;;;.
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DRAFT - PREDECISIONAL INFORMATION
The inspection also identified two inspector
followup items
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involving: (I) an unreviewed safety question concerning the use of
the alternate radwaste building, and (2) the lack of operator
guidance concerning the applicable limiting conditions of operation
during engineered safety
features actuation system sequencer
outages.
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INSPECTION DETAILS
1.0
INSPECTION OIL 7ECTIVES
Recent activities which have occurred at the Vogtle Electric
Generating Plant (VEGP) have raised concerns within the Nuclear
Regulatory Commission (NRC) as to the ability and the determination
of the licensee to operate the facility in a safe and conservative
manner. To address this concern, the NRC performed a special team
inspection to determine if the licensee operates the facility in
accordance with approvad procedures and within the requirements and
intent of the facility's operating license.
In addition to the
occurrence of specific events, NRC concerns regarding the safe
operation of the facility were heightened with the receipt of
several allegations relating to operational activities at VEGP.
The aggregation of the facts and circumstances associated with the
operational events and the allegations was viewed as a possible
indicator of a non-conservative attitude on the part of the
i
facility's operating staff which warranted the immediate initiation
'
of special inspection activities.
Because a non-conservative attitude or operating philosophy may
j
represent a hazard to the health and safety of the public, a
l
special inspection team comprising staff from the Region II Office
and the Office of Nuclear Reactor Regulation (NRR), assisted by
'
staff from the Office of Investigations
(OI), was formed to
determine the individual validity and collective impact of these
allegations on the safe operation of the facility.
The purpose of
the inspection was to determine if the licensee operates the
j
facility in a conservative and safe manner in accordance with
approved procedures,
and the intent and requirements of the
facility's operating
license.
Specifically,
the
inspection
objectives were to:
1)
kssess the operational philosophy, policy, procedures, and
!
practices of the facility's operating staff and managemenc
regarding operational safety.
)
2)
Determine the technical validity and safety significance of
,
each of the allegations and their impact on the safe and
'
conservative operation of the facility.
,
l
These inspection objectives were accomplished by the use of two
inspection teams--an operations followup team and an allegations
followup team.
The efforts of these two inspection teams were
closely coordinated; however,
they independently pursued the
obj a::tives outlined above.
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3-
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Theoperationsfollowupteammonitoredcontrolroomactivitieson(
a 24-hour basis
in order to:
(1)
evaluate the
operational 8
!
philosophy, policies, procedures, and practices of the operating 3
-
' staff . and management and- (2) determine if the plant was being'
3
.
!
operated in a safe and conservative manner in accordance with the g
!
facility's operating license.
3
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C
,
The specific inspection activities of the operations team was
described in Inspection Report 50-424/90-19 and 50-425/90-19
e
g
,.
efforts and conclusions of the allege _ti_ ops followup teams are
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described in this inspection report. " In addition, this report }
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identifies several violations 2nd $2;;..;i:1 ;;;%..;;;;; in the
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licensee's :;;reti;nci pr!!:ler, prr;r-- , and procedures.
9he-
gecificdetails==d h:;i; fe; th; ine;::ti:r trer's r---=ea= are
,
detailed in the sections that follow and in the Inspection Summary.
'
2.0
ALLEGATION FOLIDWUP
'
The
inspection team
reviewed
several
allegations
for
their
[
technical validity and interviewed licensed and non-licensed
!
personnel to determine their personal knowledge and experience
!
regarding these issues.
This portion of the inspection was
j
performed to determine the validity and significance of the
.
allegations.
5:::r:: the elle;stierr errerted *Mt
li--- ed
!
'
- t
- :: 5:d vieleted the Techair:1 Sp^cificatiene (??) vith the
!
h.:rl:d;: f lieerrer rare;r rrt, *he inepretien t:22 revier:d th: '
cirrrrrtencer e-d retienele fer i=dividerl retic- .
'
The inspection of the allegations included technical reviews of the
licensee's records, logs, and interviews of the personnel involved
in the alleged violations.
Although a transcribed record was not
required for every discussion with the licensee's staff, the
inspection team conducted sworn,
transcribed interviews with
selected individuals in order to document (1) the individual's
personal knowledge and involvement in the alleged violations and
(2) the circumstances and rationale for their individual actions.
Although an of investigator was assigned to the inspection team to
assist during the transcribed interviews, this inspection was not
an investigation into .the intent ofghe alleaed vi.olations. TwaM
ew cos ar 7w Anap Aur.sers 5 m Amp.rc h
p c. m n Cnc ,ys
s,.
r
The interviews were transcribed after the technical evaluations of
the allegations in order to permit a focused interview and to
minimize the length and scope of the transcribed proceedings.
The
transcribed interviews are listed in Appendir 1 in the order they j 4 p
were conducted.
The sworn testimony was th? 5;;;6on wnica the
inspection team reached its conclusion on each of the allegations.
i
These conclusions are prcsented in the material that follows
(Sections 2.1 through W ).
'
'
2. . B
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DRAFT - PREDECISIONAL INFORMATION
2.1
.Imoroner Installation of FAVA System
i
An allegation indicated that VEGP installed and operated a radwaste
nicrofiltration
system,
known
as
the
FAVA
system,
without
!
j
performing an adequate engineering and safety evaluation (i.e.,10
!
CFR 50.59).
Furthermore, the material configuration, fabrication
.
i
I
and quality of the system did not meet the guidance of Regulatory
l'
Guide (RG) 1.143 and the requirements of the American Society of
Mechanical Engineer's (ASME) Code.
.
1
i
The FAVA system was temporarily installed for removing Niobium-95.
The system was later determined to be better suited for as-low-as-
,
i
'
reasonably-achievable considerations during refueling outage IR2,
i
i
particularly for removing Cobalt-59 and Cobalt-60. VEGP planned to
i
replace this temporary
modification with a permanent, high-
l
j;
quality, steel system in the future; however, the health and safety
of the public may be jeopardized if a break in the system
i
(resulting in a radioactive release to an unrestricted area)
i
occurred in the interim.
'
,
,
j
Discussion
i
,
?
!
.
In February 1988, the VEGP experienced difficulty in removing
[
e
,
colloidal Niobium-95 following a reactor shutdown for maintenance
-
i
work.
FAVA Control Systems (FAVA) was hired to help rectify this
problem.
FAVA was selected because of its experience in filtration
!
j'
and domineralization.
The situation was corrected by installing
a 0.35-micron filter system downstream of the existing vendor-
-
i
supplied pre-filters.
However, a large volume of radwaste was
t
i
generated as the 0.35-micron
filters
rapidly exhibited high
i
differential pressure and were required to be changed frequently.
The need to change filters frequently also resulted in additional
!
radiation exposure to Radwaste Department personnel.
!
Upon evaluation of the performance of the 0.35 micron filter
j
system, the Radwaste Department felt that the best approach to the
problem was a back-flush, pre-coat filter system.
However, no
operational data was available for a system of this type in this
j
specific application. FAVA supplied a proprietan Ultra Filtration
System (Model No. SFD/E) for testing purposes in order to evaluate
3
whether or not this was a viable and economic solution to the
problem.
The FAVA system was installed before the Unit I refueling
i
outage and was operated under Test Procedure T-OPER-8801.
The test
j
system kept liquid effluent releases well below TS limits.
on the
basis of an evaluation of test results by the Radwaste, Chemistry,
,
and Engineering Departments, a general work order was initiated to
l
purchase a permanent system.
.
i
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!
'
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LIMITED DISTRIBUTION - Not For Public RalsoD2
4
DRAFT - PREDECISIONAL INFORMATION
l
<
1
In the early part of 1989, a Quality Assurance (QA) Department
'
audit
identified
a
significant
audit
finding
involving
a
programmatic breakdown in the procurement of the FAVA system and
!
the failure to meet commitments of the Final Safety Analysis Report
i
!
(FSAR).- Because of that finding, the FAVA system was removed from
service.
In late 1989, the licensee sought to reinstall the FAVA
,
i
system under a temporary modification because colloidal Cobalt-59
i
and Cobalt-60 had to be removed.
The Plant Review Board (PRB)
,
reviewed this temporary modification and several members expressed
]
strong objections to it based on the previous QA audit finding.
>
-
i
Subsequently, a request for engineering assistance
(REA) was
i
submitted and a 10 CFR ' 50.59 safety evaluation was performed in
i
late 1980.
This safety evaluation did not properly address the
i
guidance of Regulatory Guide (RG) 1.143 regarding the use of
polyvinyl chloride
(PVC)
piping.'
Therefore,
another safety
-
evaluation was p rformed in February 1990 to address this issue---
j
particularly with respect to radiation degradation.
'
2
l
The February 1990 safety evaluation specifically stated that the
1
FAVA system did not conform to the criteria of RG 1.143.
This
!
deviation was found to be acceptable for the following reasons:
'
!
The design of the FAVA system had been previously evaluated
'
1)
and found to be adequate in the response to REA VG-9057 dated
l
November 28, 1989 (log SG-8592).
l
2)
The location of the FAVA microfiltration system inside a
i
shielded, watertight vault provided adequate assurance that
any system failures will be contained and would not create the
l
potential for offsite releases of, radioactivity.
.
l
3)
The presence of PVC pipe in the FAVA system,
although
l-
prohibited by RG 1.143, was acceptable because the radiation
i
exposure to the plastic was within acceptable limits for up to
i
6 months based on the following:
!
a)
The amount of PVC piping used was not extensive and was
j
contained on the FAVA filter skid.
1
i
b)
There were no reported leaks or malfunctions during the
approximately 6 months that the FAVA system filter was
'
previously in use,
d
c)
Since the FAVA system filter skid was located within the
demineralizar vault, it would be protected from being
damaged.
)
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DRAFT - PREDECISIONAL INFORMATION
I
d)
On the basis of the assumed' length of time that the PVC
.
!
piping would be used in a radioactive environment and the
activity levels of the effluent at this stage in the
!
liquid radwaste process, the integrated dose to the PVC
'I
piping would be well below the radiation damage threshold
!
for PVC pipe as reported in Electric Power Research
'
i
Institute (EPRI) Report NP-2129, dated November 1981
!
(i.e., 6.5 rad over a 6 month period versus the radiation
j:
damage threshold of 5.0 x lo rad) .
s
i
e)
The PVC pipe would not be subjected to excessive pressure
!
I
conditions since the maximue. available inlet pressure to
i
i
the filter was so to 100 pounds per square inch gauge
!
(psig) which is well below the maximum allowable working
pressure of 120 psig for the PVC pipe.
,
j
f)
The system could be operated at design-basis conditions
for 182 days before it would exceed the radiation damage
i
threshold. However, under conditions currently existing
at the plant, the expected dose to the PVC piping will
.
j
less than 0.1 percent of the design basis.
i
Although the testamony of one of the PRB members indicated that the
temperature effects on the use of PVC in the FAVA System were not
,
adequately evaluated before the system was installed, the testimony
i
!
of the corporate system engineer indicated that this was considered
i
prior to installation, although not specifically documented in the
safety evaluation.
1
1
The VEGP general manager subsequently consulted the NRC resident
!
inspector to seek an NRC position with regard to placing this
1-
system - back in service.
This was supplemented by information
{
documenting reasons why it should not be placed in service.
This
'
package was forwarded to Region II and the office of Nuclear
Reactor Regulation (NRR) for review.
In March 1990, following
Region II and NRR concurrence via a telephone conference, the
licensee placed the FAVA system in service with the following NRC
!
stipulations:
I
j
1)
Procedures for operating the FAVA system required an operator
to be in attendance for the entire length of time the systra
,
j
would be in operation.
-
'
i
.
2)
All hoses going to and coming from the FAVA syst en required
!
verification that they met the requirements of RG 1.143.
1
3)
The cover over the FAVA system wa- required to be securely
fastened when the system was in operation to ensure that if a
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_ _ _ _ _ _ _._ -_ __ _______ _ ____
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DRAFT - PREDECISIONAL INFORMATION
-
!
i
spraying leak developed, it would be contained in the concrete
l
vault.
i-
4)
The design of the . walls of the alternate radwaste building
!
(ARB) was required to be evaluated to determine whether or not
!
i
a design modification should be made to reduce the potential
?
j
of wall leakage in the event that a hose leak developed and
j
sprayed its contents on the walls.
,
i
In June 1990, in response to item 4 (above), the licensee revised
Part G of the safety evaluation for the FAVA system.
Part G of the
i
safety evaluation addressed the effect that operation of the FAVA
1
!
system would have on the probability of occurrence or consequences
,
{
of accidents described in the FSAR.
Although there was no
comparable accident analysis in the FSAR that addressed the ARB
4
accidents or the consequences of accidents in the ARB, the FSAR
I
accident analyses (Chapters 15.7.2 and 15.7.3) did describe worst-
case releases of the contents of the recycle holdup tank (HUT) .
l'
The first bounding analysis in Chapter 15.7.2 addressed the release
of the entire gaseous radioactive contents of the HUT to the
{
i
environment at ground level and the second bounding analysis
'
addressed the release of the entire liquid contents of the HUT-
i
through an assumed crack 2n the ARS floor directly into the ground
- .
water supply.
In both cases, the 10 CFR Part 100 and 10 CFR Part 1
'
20 limits were not exceeded.
These criteria were consistent with
'
j
criteria provided in NRC Circular 80-18, "10 CFR 50.59 Safety
Evaluations for Changes to Radioactive Waste Treatment System."
'
However, neither of these analyses addressed the potential for wall
spray down and leakage. through the ARB walls and the subsequent
t
release path to the environment.
Therefore, the licensee revised
the safety evaluation in June 1990 to address the consequences of
a hose break on the FAVA system which would result in wall spray
i
l
down and potential leakage to the environment.
,
l
The inspection team's review of the revised Part G of the safety
i
evaluation identified several erroneous assumptions with respect to
the release path and the dilution volumes that could be used in the
analysis of a hose break and resultant wall spray down.
However,
,
the inspection team also found that the design of the FAVA system
(i.e., the use of a system cover) would prevent wall spray down and
that the only potential source for wall spray down and subsequent
leakage was from a hose break in another radwaste system in the
ARB. Therefore, the inspection team concluded that the FAVA system
safety evaluation dated June
1990,
adequately addressed the
.
temporary modification for the installation of the FAVA system;
j
however, the inspection team's review identified an unreviewed
4
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DRAFT - PRIDECISIONAL INFORMATION
safety question concerning the release paths and consequences of a
failure of the other radwaste systems in the ARB.
In' addition, the team noted that in Supplements 3 and 4 of the
Safety Evaluation Report (SER), the NRC staff reviewed and accepted
the design of the ARB and specifically addressed the consequences
,
,
of a hose break on a radwaste system in the ARB.
However, the SER
supplements addressed the effects of high airborne activities and
puddling and did not address the potential for wall spray down and
,
leakage.
The ARB was installed before the plant was licensed;
t
therefore, the NRC approved the design and use of the ARB in
'
)
Supplements 3 and 4 of the SER.
Thus, there was no requirement to
!
perform another evaluation of the potential effects of hose brcaks
on systems other than the system being installed by the temporary
1
modification (i.e., the FAVA system).
Because the design of the
FAVA system effectively prevented a wall spray down, this was not
a concern that was required to be addressed by the FAVA system
'
'
safety evaluation.
Nevertheless, now that it has been identified,
l
the consequences of a hose break and wall spray down in the other
ARB radwaste systems must be resolved.
Therefore, this issue will
4
be followed as an inspector followup item pending further review
and evaluation and is identified as:
19 -14
19 - N
- '
IFI 50-424/90.x*-07 and 50-4 2 5/ 9 0-xw-02",
'Dotential Unreviewed
Safety Question Regarding Spray Down of the Alternate Radwaste
Building."
.
J
<
Conclusion
Although the FAVA system was originally installed without an
adequate safety evaluation and did not meet the regulatory
3
guidance, the inspection team concluded that the subsequent safety
i
evaluations were acceptable for the system's use.
Serefert, th;
)
inerrtien tem cen:1 d:d that th; ellgeti;n iter ne*
M 1y
(
1
'
r Arte el.i d.
As a result of QA Department's significant audit finding in early
1989 involving a breakdown in procurement and failure to meet FSAR
commitments, the system was removed from service.
Subsequently,
the FAVA system was returned to service following two safety
j
evaluations which adequately addressed the use of PVC piping with
,
respect to radiation degradation and pipe rupture.
Therefore,
these safety evaluations justified the use of the FAVA system, even
though the recommendations of RG 1.143 and ASME Code requirements
were not met. Although the safety evaluations did not specifically
address high-temperature effects, the testimony indicated that
these effects had been considered before the system was installed.
i
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13
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i
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.-
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DRATT - PREDECISIONAL INFORMATION
Although the safety evaluation performed in June 1990 at the
request of the NRC Region II Office did not adequately evaluate the
,
!
effects of a wall spray down and wall leakage to an unrestricted
area, this evaluation was not required because the FAVA system has
a protective cover and the use of hoses and effects of hose breaks
(i.e.,
airborne activity and puddling) were addressed in SER
J
Supplements 3 and 4.
I
Regardless of whether the safety evaluation was required to address
the effects of a break in the hoses (which could result in wall
spray down or leakage), the inspection team identified a new
concern involving the use of the ARB because the safety evaluation
inadequately addressed the potential effects of wall spray down
l
from any other source in the ARB owing to erroneous assumptions
concerning the release path and the dilution volumes.
This is a
potentially unreviewed safety question concerning the use of the
<
alternate radwaste building.
2.2
Operability of the Residual Heat Removal Pumo
An allegation indicated that during Unit i refueling outage IR2
'
(RHR)
Train A out of service for
maintenance, the Train B RHR pump experienced excessive vibration
and a nuclear service cooling water (NSCW) motor cooler outlet
i
leak.
In addition, TS 3.9.8.1, "RHR and coolant Circulation," was
i
allegedly violated because the operations Department chose not to
declare RHR pump 15 inoperable in an effort to mitigate the impact
,
on the critical work path.
Discussion
TS 3.9.8.1 requires at least one RHR train to be operable and in
operation during Mode 6 (refueling) when the water level above the
top of the reactor vessel flange is 23 feet or more.
Otherwise,
,
'
Suspeed all operations involving an increase in the
reactor decay heat
load
or
a
reduction
in
i
,
concentration of the reactor coolant system (RCS) and
j
!
Immediately initiate corrective action to return the
'
I
required RHR train to operable and operating status as
soon as possible and close all containment penetrations
'
providing direct access from the containment atmosphere
to the outside atmosphere within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />.
The inspection team verified that during Unit I refueling outage
IR2 with higher than normal vibration measurements on the RHR pump
<
1B and a leak on the NSCC outlet of the Rh motor cooler,
4
operations
Department
personnel
did
not
declare
the
pump
'
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,
i
i
This determination was made after consulting with the
on-shift duty engineer from the Engineering Department and was
!
,
based on the determination that the pump would fulfill its intended
j
safety function in Mode 6.
Specifically, the RHR pump was capable
'
!,
of removing decay heat from the partially defueled reactor core.
j
The testimony of the individuals involved indicated that this
.
.
operability determination was based on the fact that the vibration
readings taken at the inservice test (IST) surveillance points did
not reach the IST Alert levels and were therefore acceptable for
continued service. Although the high vibration readings on the top
end of the RHR pump
were
later determined by
the
vendor
.
(Westinghouse) to be excessive, at the time of the operability
i
-
evaluation, the licensee accepted these values, regardless of their
f
magnitude, because the readings at IST test points were below the
I
Alert levels. The testimony also indicated that, even with a leak
l
l
on the NSCW outlet of the RHR motor cooler, the motor was receiving
'
j
full cooling water flow and cooling would not have been immediately
i
compromised following a complete NSCW discharge pipe break.
l
Furthermore, the. testimony indicated that the operations Department
j
had : implemented compensatory actions to monitor the vibration
levels and NSCW 1eakage and ensure the continued operability of the
l
pump by stationing an operator at the RHR pump to monitor the
vibration levels and notify the control room if the vibration
levels increased, thus allowing the control room to implement the
,
actions of the limiting condition for operations (140).
The inspection team also noted that in event of a catastrophic
i
!
failure of the RHR pump, all the required actions of TS 3.9.3.I
I
'
(i.e.,
closing all containment penetrations)
could have been
completed within the required 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> time period of the 140 because
$
the Ito for TS 3.9.4, " Containment Building penetrations," was in
-
'
effect during this time period.
This LCO was implemented due to
the movement of irradiated fuel from the core to the spent fuel
,
j
pool.
The 140 required that,
4
The equipment door be closed and held in place by at
least four bolts; at least one door in each airlock be
closed; and each penetration providing direct access from
1,
the containment atmosphere to the outside atmosphere
i
shall be either closed by an isolation valve, blind
.
flange, or manual valve, or be capable of being closed by
'
an operable automatic containment ventilation isolation
j
valve.
4
As a result of the implementation of TS 3.9.4, the only remaining
act' .n for the LCO of 73 3.9.8.1 would have been to close the
}
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containment purge valve which receives an automatic closure signal
'
and could have been isolated within the Iro action times.
!
During the course of this review, the inspection team found that
4
the licensee failed to initiate a deficiency card for either the
!
i
NSCW 1eak or the excessive vibration as required by operations
!
Procedure 00150-C, " Deficiency Control."
This procedure requires
i
4
i
that a deficiency card be written if the deficiency involves
'
i
safety-related components which are to be dispositioned "use-as-
i
is/ repair," or other conditions involving safety-related components
,
which require engineering suppolt or other technical assistance to
i
determine if the component is deficient.
Failure to establish,
implement, and maintain adequate operating procedures represents a
,
,
1
violation of TS 6.7.1.a.
This item is identified as:
R-G
6
I
.'
VIO 50-424/90_xx=Gt,i..a ;; = /;0 m ;i, " Failure To Establish or
l
Implement Procedures for Required Activities."
h
conclusion
,
!
!
The inspection team c
luded tht t.5e
11-v. tis, n; n;t frily
'
i
c ertentistrf L;;.;;.3
e operations Department had an adequate
i
engineering basis for accepting the operability of the RHR pump in
!
j
spite of the pump's deficiencies.
In addition, the team concluded
i
j
that declaring the pump inoperable would not have impacted the
!
critical work path: the 140 actions would not have been restrictive
because containment (excluding ventilation) had been isolated as
'
required by TS 3.9.4.
The LCO actions would not have prev . ,ad the
,
,
continuation of refueling activities because the actions to close
!
all containment penetrations providing direct access from the
containment atmosphere to the outside atmosphere would only have
1
required closing the containment purge valve which has an automatic
closure signal.
l
In addition, the inspection team identified that the licensee
violated the station's administrative procedures by failing to
initiate a deficiency card for either the NSCW outlet leak or the
,
excessive vibration on the RNR motor as required by Operations
Procedure 00150-C.
'
t
-?'
"!:rrf cert fr ent I:02: tier V:1:: Ourec ill;; ca
-
,
l
An allegatio
icated that a unit
shift
isor
(USS)
concealed the correc
time for a T
o prevent a forced
i-
shutdown of the unit and to
CFR 50.72 notification to
'
the NRC.
Furthermore, c
ent
. ion valves (CIVs) which
were missed durin
rveillance test sho
va been declared
'
!-
inoperabl
e immediata actions of the TS LCO s
ave been
1
i
at the time the missed surveillance was identifie .
1
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DRAFT - PREDECISIONAL INFORMATION
.
i .
ddition, delaying the initiation of the deficiency card (DC) unt 1
t
surveillance had been re-perfonned allowed the licensee
o
i
av (d the immediate actions of the LCO and allowed the un
to
i
)
rema'in in operation and avoid the immediate NRC notificatio .
Discus
on
!
The inspe tion team reviewed the documentation of
a missed
j
surveillanc
on the containment isolation valves
escribed in
a
Licensee Eve
Report (LER)90-001 for which a non-
ted violation
(50-425/90-01- 1) was issued.
The LER identified
hat during the
i
review of mont y Surveillance Procedure 1447 -2,
" Containment
!
Integrity Veriff
tion-Valves outside Contain
nt," the licensee
>
'
discovered that 3
CIVs had been overlook
and had not been
i
tested.
In additi
the valves had not b en tested during the
,
previous two month 1 s surveillances.
Up
identification, the
<
j
operating
shift
re-performed
the
com
ete
surveillance
and
initiated an investigat
n which resulte
in a deficiency card (DC)
!
for the previously misse
surveillance .
i
i
The LER indicated that t
root cause of the violation was
,
8
personnel error in reviewing t e co
lated surveillance task sheet.
i
In addition, the computer softv
which generated the surveillance
l-
task sheets (STS) has been a
ified so that it is no longer
!
possible to inadvertently
t
n
incomplete listing of the
'
equipment.
Even if an error
imil
to the one which resulted in
only two valves being shown n the S
were to recur, it could only
.
result in either all or n
e of the e
ipment being listed,
i
The
inspection team v rified
that
S
3.6.1.1,
" Containment
!
Integrity," 140 actio
statement requi
d restoring containment
l
integrity within 1
ur or commencing
unit shutdown to hot
standby within the n t 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />.
A shutdo
required by Technical
-
Specifications wou d have required that th
NRC be immediately
.
notified in accor ance with 10 CFR 50.72.
s
!
'
The inspection aan found that the CIV surveillance requirement of
i
TS 4. 6.1.1. a
ad been completed and approved.
The surveillance
procedure r
ired verification every 31 days that al penetrations
,
i
not capabl4 of being closed by operable containee t automatic
i
isolation / valves and
required to be
closed durin
accident
conditi ns be closed by valves, blind flanges, or d
etivated
)
autom
ic valves secured in their normal positions.
Du ing the
'
next
shift,
the
oncoming
shift
supervisor
noted
th
the
elllance procedure was only partially performed and that 9 of
su
'
t
CIVs on the surveillance procedure had been marked as
ot
pplicable" and had not been performed.
'
a
.
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TS\\.0.2.a requires that each surveillance requirement be perforud
witft4n the specified time interval
with a maximum allowa ee
exten) ion not to exceed 25 percent of the surveillance inte
In aditition,
requires
that
failure
to perf
a
al.
survell
nee requirement within the specified time interva
shall
constitut
a failure to meet the operability requirement
for an
LCo.
As
uch
the failure to perform Surveillance R
irement
4.6.1.3.a fk a,ll the CIVs within the surveillance pari
(i.e. , 31
days plus the 25-percent extension) would have co
tituted an
inoperable con' ition of the CIVs.
The oncoming USS
stified that he lacked sufficie
information to
determine if the
omplete surveillance had n
been performed
within the survalliance frequency because he w
not familiar with
the
circumstances under which the surveillance procedure was
performed.
Furthermorg, he lacked sufficient information in the
control room to deterni e if the complete. surveillance procedure
had been performed within
he surveillance ' period. On the basis of
his experience, the CIV su
eillance was mormally performed in its
entirety; therefore, the potential existed that another partial
surveillance procedure had verified the position of the missed
CIVs.
Although
the control room,previously performed surveillances were filed in
these records' era for information only and were
neither controlled nor complete.
'
'
The USS indicated that the previou stwo monthly surveillances on
the CIVs obtained from this ' file sqre performed incompletely;
however, he did not know whether surveillances on the missed CIVs
had been performed completely under \\some other surveillance
procedure.
This was confirmed when tNe team interviewed the
surveillance coordinator! Who indicated that approximately once a
missed surveillances were performed under different tasks. mo
Upon identificatiop/
\\
of the potential missed surV illances the USS
initiated an inveftigation to determine whether the surve,illances
t
had actually b en missed and,
concurrently,
r -performed the
surveillance w hin three hours. The inspection tea verified that
the discove
time on the deficiency card correctly
flected the
time at whi
it was verified that the previous two s
had been p
formed incompletely.
elllances
Cone
sion
On the basis of the testimony of the USS, the inspection te
,
neluded that the allegation was not fully substantiated becaus
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USS did not conceal the true discovery time of the sis
surve
ces to avoid a unit shutdown.
The USS indi
that he
was not pre
ed to keep the plant in operation
o prevent NRC
'
notification.
stated that he had
er been given any
indication or instruc
to do " wha
r it takes" to kecp the
unit on line or to avoid N
t
ation of unusual events.
The
USS did not know and co
no
onfirm if the previous CIV
surveillances had been
equately per
ed and believed that the
surveillance co
re-performed within
allowable outage
time; ther
, his actions to initiate an invest
on into the
4
adequ
of the previous surveillance and to concur
re-
"
ora the CIV surveillance procedure were appropriate.
- :
":f: chance 9fth Inemable source -Jtanae- Monitor Mucien
f
Instrument
1
1
An al
gation indicated that the operations
staff allege
'
knowing
violated Technical Specifications (TS) when the uni
as
taken fro
Mode 5 (cold shutdown) to Mode 6 (refueling)
th a
i
source rang monitor (SRM) nuclear instrument inoperable
d that
the prohibite operational mode change was made in orde
o reduce
the critical pat outage time.
!
Discussion
i
'
The inspection team rev
ved the documentati
of the mode change
described in Licensee Eva
Report (LER) 90
04 for which non-cited
'
Violation 50-424/90-10-03
s issued.
e LER indicated that TS 3.0.4 was violated on March
1990,
en Unit 1 entered Mode 6
from Mode 5 with an 140 for Sou
e Ra .ge Channel IN31 in effect to
allow performance of an 18-mont
'hannel calibration.
The LER
indicated that the root cause to
t
avant was personnel error by
the shift superintendent.
The inspection team confir'med that TS 310.4 required that entry
into an operational mode not be made unlesssthe conditions for the
'
i
LCO are met without aeliance on the provisions of the action
.
requirements.
With.one source range monitor inoperable, TS 3.9.2,
" Instrumentation,' could not be satisfied in\\ Mode 6 without
reliance on the' action statement.
'
/
Personnel w[re interviewed to (1) confirm the effect on the outage
schedule /irectly attributed to this TS violation, (2)
etermine
d
whether'it was known at the time of the mode change that
mode-
i
restraining LCO was in effect, and (3) determine the exte t of
phasis on schedule.
,
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G
_. - _ _ _ _ _ _ . _ _ . . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ ,
_
_ . - _ . _ . ._
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._._._._ _ ._ _ _._ _ _ _ _ _ _ _. _ _
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/
!
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I
.
The testimony and a review of the outage schedule confirmed tha
(
ere was a reduction in critical path outage time which w
!
d
ectly attributed to proceeding to Mode 6 before restoring /
the
l
!
o an operable status.
l
i
.
i
l
The te
isony also indicated that the shift superintendent (SS) and
{
.the uni
shift supervisor (USS) did not recognize that 'a mode-
j
restrain
LCO was in effect at the time of the mode change.
Both
!
the SS and
SS were aware that there was an active 140 on the SRM,
,
but neither
f them had connected the LCO to the mode., restriction.
i
contributing
ctors to the error were that both th
8 and USS had
i
directed their attention to a problem with the
esting of the
)
engineered safet
features actuation system (ES
) sequencer and
i
i
that the-work whi
had been emphasized to be
1 ding up the mode
!
change was the d ontamination of the
redctor head.
Upon
i
<
j
notification that th
Health Physics Department had cleared the
l
reactor head for work, the SS granted permission to enter Mode 6.
i
i
The testimony also indic
ed that there 'was no indication of an
,
i
unreasonable emphasis on t
critical path schedule.
Both the SS
-
and USS indicated that they had never been given any indication or
'
!
instruction to do "whatever i
takes" to stay on schedule.
They
also indicated that they did
t , feel undue pressure to stay on
'
I
schedule and, particularly, not
!
, f it meant compromising safety.
,
,
/
!
The SS admitted that he was initia ly commended for the schedule
'
j
benefits; however, the violation of
he Technical Specifications
'
was not recognized at the time.
Thg SS indicated that he had
initially received some
sitive fee
ack during the morning
.
!
management briefing for
a shift's acco
lishments and later in
!
the briefing the TS vio ation was recognize and discussed. In the
l
SS's opinion the re
nition of the TS
olation negated all
positive feedback.
,
a
]
The inspection t an identified an additional c cern during the
'
inspection conc ning the format and use of the
status sheets.
On the basis
interviews with the SS and USS a
the review of
the format o the 140 status sheets, the inspection
as concluded
i
that both
a format and normal use of this form co
ributed to
this TS v lation.
i
The LC status sheet, is a two-sided form; the section for
quired
j
actio a begins on the front and continues on the back, who
the
"re
rks" section is located.
During the testimony, both t
i
USS indicated that their usual practice, notwithstanding a
an
e
anges, was to review only the front of this form because onk
restorative actions were noted on the back.
In this case, the mode
1
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!
estraint was noted on the back of the form in the " remarks"
se
ion.
,
l
LER 90
4 did not identify the format and use of the LCO st
us
sheet, as
cause of the violation
therefore, corrective
ions
,
have not ye
een i:aken in this regard.
The failure to
dentify
,
and implement dequate corrective actions to preclude repetition is
a violation of l'O.CFR 50, Appendix B,
Actions," and as s(uch will be followed as: Criterion XVI/ " Corrective
VIO 50-424/90-xx-03,
"F
ure To Determine and' implement Adequate
,
s
Corrective Actions."
'
N
!
Conclusion
'
j
onthebasisofthetranscribed,Jnkerviewsandfromitsreviewof
)
,
the outage schedule,
the i
pectionsteam concluded that the
allegation was not fully s
stantiated. N.The testimony indicated
'
that the mode change w
a critical pathsites.
However, the
testimony of the shift
perintendent and the unit shift supervisor
involved indicated that at the time of the mode' change they were
not aware that an'Ir0 was in effect on the SRM a
that a mode
change was pro
ited.
The ins
ion team also concluded that the corrective act
ns for
the
failed to identify that the format and use of th
140
sta
sheets, was one of the causes of the event.
Therefore,
e
f
ure to implement appropriate corrective actions was found to
violation of 10 CFR 50, Appendix. 8, Criterion XVI.
,
2.b pr Backdatino of sianatures
An allegation indicated that a temporary change to Abnormal
Operating Procedure (AOP) 18028-C, "Ioss of Instrument Air," was
not approved within the 14-day requirement of TS 6.7.3.c; and that
the unit superintendent intentionally incorrectly signed and dated
the temporary change to indicate that the TS requirement was
'
satisfied.
,
j-
Discussion
TS 6.7.3.c requires that temporary changes to AOPs which do not
involve changes to the intent of the original procedure be
documented and reviewed in accordance with TS 6.7.2 and approved
4
within 14 days of implementation.
TS 6.7.2 requires that changes
to AOPs be reviewed as stated in administrative procedures and
approved by the Plant Review Board (PRB) and gener11 manager.
Administrative
Procedure
00100-C,
"Cuality Assurance
Records
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_ _ _ _ .
_ _ _ _
_ _ _ _
_ _ _ . . _ . _ . . _ . _ _ _ . _ _ . _ _ _ _ . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ . _ _ .
e
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Administration," Paragraphs 4.1.1.4
and
4 .1.1. 8,
require ~ that
'
i
corrections to Quality Assurance records exhibit necessary and
appropriate signatures, initials, and dates.
!
i
operations Procedure 18028-C, Revision 7, provided operator actions
in the event of a loss of the instrument air system.
A temporary
'
.
j
change to the procedure was initiated on May 29, 1990, to delete
i
the references to the header isolation at 70 psig and the
i
associated actions.
This change was processed in accordance with
Administrative
Procedure
00052-C,
" Temporary
Changes
to
i
Procedures," which allowed the temporary implementation of minor
i
changes to procedures as long as the change was approved by the PRB
j
j
and signed by,the general manager within 14 days of the temporary
'
change. Therefore, Temporary Change Procedure (TCP) 1802-C-7-90-1
)
was required to be approved by the PRB and signed by the general
,
manager by June 12, 1990.
'
'!
l
The PRB tabled the TCP on June 8,
1990, (PRB meeting 90-81) and
i
j
assigned action to the Operation's Department to void the TCP or
revise the TCP to incorporate the PRB comments.
Revision 8 to
]
Operations Procedure 18028-C was developed to modify valve numbers
and descriptions reflected in Temporary Modificatiors 1-90-006 and
i
2-90-002.
This revision superseded the changes of the TCP.
On
i
June 12, 1990, the PRB approved Revision 8 (PRB meeting 90-82) and
!
the TCP was removed from the control room copies of the procedure.
]
On June 15, 1990, the unit superintendent lined out the operations
.
manager's previous approval of the TCP and marked the TCP form as
!
disapproved by the operations Department.
The date entered on the
!
form was June 12, 1990.
I
j
On June 22, 1990, the PRB secretary initiated Deficiency Card (DC)
1-90-282 which indicated that the unit superintendent incorrectly
i
dated the TCP with the date of June 12, 1990, rather than actual
date of June 15,1990, and DC 1-90-283 which indicated that the TCP
j'
was not processed within the required 14 days (i.e., by June 12,
1990).
The resolution of these DCs, the associated PR8 meeting
,
i
minutes, and discussions with the operations manager and Nuclear
Safety and Compliance Department staff indicated that described
deficiencies were acknowledged and confirmed by the Operations
!
Department on July 3,1990, and attributed to personnel error. The
I
TCP form was dated with the date on which the Operations Department
l
decided to void the TCP and not the date on which the original was
j
actually signed.
l
As part of the corrective actions for DC 1-90-282, a TCP record
correction notice was initiated to correctly indicate the date on
'
,
!
which the TCP fo11 was pro..ssed;
however,
tus TCP record
l
correction notice could not be produced--one was subsequently
,
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written on August 14, 1990.
In addition, the operations manager
4
- -
counselled the unit superintendent and assigned him to investigate
!
both DCs because he was the most knowledgeable of the deficiencies
and the assignment served to reinforce the reprimand.
The
'
subsequent PRB meeting of June 28,
1990,
(PRB meeting 90-90)
4
determined that the 14-day TS violation addressed in DC 1-90-283
.
was reportable to the VEGP vice president, but not to the NRC.
1
However, the inspection team found that the report to the VEGP vice
i
president was not made.- On August 9, 1990, the PR8 (PRB meeting
} .90-104) confirmed that the report was required.
As of August 17,
!
i-
1990, ~ the licensee had not issued the required . cport to the VEGP
j
vice president; however, the licensee intended to issue the report.
>
,
With respect to the rationale for the unit superintendent's
actions, the inspection team learned (during discussions with the
'
}.
Technical Support Manager) that the PRB secretary told the unit
i
superintendent on June 15, 1990, that the TCP needed to be voided
and 4 DC written for violating the 14-day requirement of TS 6.7.3.
l
As discussed in Section 2.11 of this inspection report, Operations
i
Department personnel are held personally accountable for violations
' -
and LERs
(i.e., there is a direct impact on their bonus pay);
therefore, a reportable occurrence based on this event could have
!
i
adversely impacted the unit superintendent's salary.
l
l
The testimony of the unit superintendent indicated that he dated
the TCP with the date (June 12, 1990) on which the PR8 disapproved
I
it and not the date on which it was actually signed (June ' 15,
i
1990).
Additionally, the unit superintendent had no recollection
l
of any discussions on June 15, 1990, regarding violation of the 14-
l
day TS requirement. He indicated that he never considered the 14-
day requirement despite his previous
knowledge and training
i
concerning this requirement and the June 12, 1990, expiration date
'
indicated on the TCP form.
i
!
The testimony of the PRB secretary
indicted that during a
!
discussion with the unit superintendent on June 15, 1990, she
'
identified the need to void the TCP, as well as the need to write
'
!.
a DC for violating the 14-day TS requirement.
Therefore, the
inspection team was concerned about whether the TCP was voided
j'
before or after the PRB secretary identified the need to void the
!
In order to resolve this discrepancy, the
'
inspection team discussed the discrepancy with the PRB secretary on
August 16,
1990.
In addition to earlier testimony, the PR8
,.
'
secretary indicated that during her discussions concerning the TCP
'
with
the
unit. superintendent
on
June
15,
1990,
the
unit
'
superintendent had indicated that the TCP had already been voided
j
aar13 : in the day.
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conclusion
i
l
On the basis of the testimony, the inspection team concluded that
backdating to avoid a violation of the 14-day TS requirement was
I
not '0117
="h-"-ti tted
idditi^=,
the
r^ cer- th t ibis
T=
i
practice
m-
a plant-wide problem,==-
et
- "11 y =nh=* =-t itt ed .
However, the inspection team did confirm that TCP 1802-C-7-90-1 had
i
!
been dated incorrectly; this was a violation of Administrative
i
Procedure 00100-C, " Quality Assurance Records Administration,"
!
Paragraphs 4.1.1.4 and 4.1.1.8 and will be followed as:
!
19-l's
tq -G
VIO 50-424/90-xx-@2' and 50-425/90-mm-er, " Failure to Establish or
\\
'
1
l
Implement Procedures for Required Activities."
l
g y Reportability of Previous Enaineered Safety Features Actuation
System Load Seauencer outaaes
!
<
An allegation indicated that the operations Department incorrectly
l
used a 72-hour shutdown requirement when one of the two ESFAS load
sequencers was previously inoperable.
It was also indicated that
l
VEGP had taken no action to ensure that the past occurrences were
,
l
identified and reported to the NRC as required by 10 CFR 50.73,
j
despite newly acquired information that deenergizing an ESFAS
i
sequencer required entry into the 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> limiting condition for
.
operation (Iro) action requirements of TS 3.0.3.
In addition, the
l
possibility existed that the 140 for TS 3.0.3 (i.e. , 7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br /> to hot
standby)
were exceeded when
the
sequencers
were
previously
.
i
deenergized for maintenance and testing. This concern was based on
(1) the
lack of a specific TS for the
sequencers,
(2)
the
'
operations Department historically linking the sequencer outages to
!
the emergency diesel generator (EDG) 140 of TS 3.8.1.1.b (78 hours9.027778e-4 days <br />0.0217 hours <br />1.289683e-4 weeks <br />2.9679e-5 months <br />
to hot standby), (3) a limited review of past maintenance work
,
i
orders (MW0s) indicated possible sequencer deenergiration; and
(4) comments by the engineering staff that the sequencers had been
'
previously deenergized.
Discussion
l
There are two ESFAS sequencers for each unit--one for each 4.16-
kilovolt (kV) emergency bus.
Each sequencer is activated by one of
e
!
two conditions, undervoltage (UV) on the associated emergency bus
!
or a respective train's safety injection (SI) signal. Upon receipt
i
of either or both of the initiating signals, each sequencer will
j
perform all or part of the following functions:
Start the associated EDG.
'
'
I
i
j
Stop any test sequence in progress.
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Strip the associated emergency bus of all loads (UV
j
i
only).
close the associated EDG breaker (UV only).
[
Energize
the
associated
train's
engineered
safety
features (EST) loads as determined by the initiating
j
signal.
l
Each ESFAS sequencer contains three levels of UV detection and
system response, as well as the power supply for this UV circuitry.
j
Four potential transformers monitor the emergency bus voltage for
}
these three levels of degraded bus voltage (Invel 1, 5 70 percent:
Level 2, 5 86 percent; and 14 vel 3, 5 88.5 percent) and furnish an
analog signal to three sets of four bistables located in one of the
five sequencer cabinets.
4-
.
!
Level _1 is the " loss of voltage" and Level 2 is the " degraded
!
voltage" which is referred to in TS Table 3.3-2,
Items 6.d, 8.a.
i
and 8.b.
As these TS items (applicable in Modes 1 through 4) do
i
not address the loss of all four channels in Level 1 or in Level 2
i
(as would be the case when the sequencer is deenergized), TS 3.0.3
would apply if such a loss were to occur.
It should be noted,
i
however, that if the sequencer were deenergized, it could not
respond to a safety injection signal either.
Therefore, there
would be only one automatic safety injection actuation channel
!
(i.e., associated with the unit's unaffected sequencer) and Item
i
1.b of TS Table 3.3-2 (6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> to hot standby) would be the most
l-
limiting 140.
1
';
Discussions with the operations manager, the assistant general
i
manager-plant support, and system engineers for the ESFAS and
,
sequencers confirmed that the Operations Department historically
'
i
linked the sequencer outages to the emergency diesel generator
2
(EDG) 140 of TS 3.8.1.1.b (78 hours9.027778e-4 days <br />0.0217 hours <br />1.289683e-4 weeks <br />2.9679e-5 months <br /> to hot standby) . Although the
)
applicability of TS Table 3.3-2 and TS 3.0.3 to sequencer outages
l
had been recently identified, past sequencer outages were not
reviewed.
Therefore, with the assistance of the licensee, the
i
inspection team reviewed the completed MWOs which were performed on
'
the sequencers on Units 1
and
2,
as well
as the
related
4
i
Instrumentation and control (I&C) , Engineering, and Operations
1
Department surveillance tests.
-
,
)
The review of completed MWOs did identify several instances where
,
i
the work performed would most likely require the sequencers to be
deenergizedt however, the associated unit was found to have not
,
been in Modes 1, 2, 3, or 4 at the time the work was performed.
.
.
Somewhat = related to this concern, the review did identify two
4
-
LIMITED DISTRIBUTION - Not For Public Release
j
25
,
!
!
.
4
.
-
-
.
e
__m. _ _ . _ _ _ _ _ _ _ _ _ _ _ _ ,
-
- -
. - - -
_ -_
_
_
_.
_ _
__
_ _ _.__ _ _ _ _ __ _ __ _ _ __ ._
_
=
, .
1
i
LIMITED DISTRIBUTION - Nat For Public R21ecco
.
DRAFT - PRIDECISIONAL INFORMATION
,
.
occurrences (March 4 and June 17, 1987) where the Unit 1 Train B
l
sequencer was inoperable during the change of sequencer controller
card A (SI4T A4-3) .
Specifically, when the controller card was
4
j
removed, both the automatic SI function and UV function for the
sequencer were rendered inoperable.
Because the unit was in Mode
i
3 (hot standby) during these two occurrences, the sequencers and
the ESFAS were required to be operable per TS 3.3.2.
However, the
i
associated 140 status sheets (1-87-354, dated March 4, 1987 and 1-
I
87-566, dated June 17, 1987) only recognized TS I40 3.8.1.1.b as
being applicable to the outage.
Despite the fact that 140s
associated with TS Table 3.3-2 (Item 1.b) and TS 3.0.3 were not
,
recognized,
these TS were not violated since the system was
-
j
. restored within 30 minutes and 10 minutes, respectively, f1F
i
' fditie ,
2- ran unit rerrin:d in 5:t Ot:nry,
pert:tility "adar
_
4
j
- ^ 07
00.72 w 00.73
- n;t r:';;ir:d [i.:., there
t'
pr:r
.
r=A n<-+ 6 ihil: 1. 2 TS LOO (10 OFP 50.?2) ner we
G. piani.-aken
I
j
te hat utandhy er : :::Olt ;f e TO LOO (10 m 50. H ) F.
1
,
i
similar to the MWO review, the inspection team's review of related
I&C, Engineering, and Operations Department's surveillance tests
l
did not find any examples of the sequencers or the ESFAS being
l
deenergized in Modes 1 through 4.
Completed 18-month ESFAS channel
i
calibrations, EDG tests, and ESTAS tests were verified as having
i
been done in Modes 5 and 6.
Completed quarterly testing of the
i
ESFAS Auto SI K610 slave relay, which removed the automatic SI
signal to the sequencer, were verified to be performed within time
i
limits allowed by TS 3.3.2.
All other sequencer testing that used
l
installed test circuitry is automatically bypassed on an SI or UV
signal.
4
i
In
addition to
the
inspection
team's
review
of
MWos
and
,
l
surveillance test
procedures,
the
system engineers
for the
i
sequencers and ESFAS [as well as the nuclear steam supply system
(NSSS) supervisor) were asked if they knew of any time in which the
4 -
sequencers were deenergized in Modes 1 through 4.
None of these
'
engineers remembered any such occurrences.
)
'
A
review
of
applicable
operator
treining
material
(System
Description 8b for Engineered Safety Features System Sequencers)
.
'
revealed that there was no reference to ESFAS TS 3.3.2, just those
for the diesel and other power sources and distributions (i.e., TS
i
3.8.1.1,
and TS 3.8.3.2.).
This finding, along with the March 4 and June 17, 1987, occurrences
l
discussed
above,
indicates
that
the
operations
Department
historically has not linked sequencer outages to the 140s of TS 3.3.2 or TS 3.0.3.
Nevertheless, discussions with the operations
~ manager and the licenced operators on shift indicated that although
,
no
written
guidance
or
TS
interpretation
existed
for
the
,
LIMITED DISTRIBUTION - Not For Public Release
,
,
26
,
!
-
,
'
_
-
-
-
.
_ . . .
_ _
_ _ _ .
. _ _ _
__
. - _ _ _ _
__
___ _
_ _ _ _ _ _ _ . _ _ _ - _
-
.
!
>
..
<
LIMITED DISTRIBUTION - Not For Public Rslease
.
l
,
DRAFT - PREDECISIONAL INFORMATION
l
sequencers,
the
operations
Department
staff
would
currently
!
consider all applicable TS requirements, including TS 3.3.2 and
j
3.0.3.
!
Conclusion
The 140 actions of TS Table 3.3-2,
"ESFAS Instrumentation," are
]
applicable for determining the operability of ESFAS components;
'
however,-if a load sequencer is not operable, the more restrictive
i
requirement of TS Table 3.3-2, TS 3.0.3, or the affected system Iro
'
i
should be considered.
Although the EDG LCO of TS 3.8.1.1.b had
been used for sequencer outages in t.he past, the allegation's
'
concern of possibly exceeding the 140 for TS 3.0.3 when the
.
sequencers
were
previously
deenergized yM
not
5:
';11y
,
}
c'2:t: .tiatad. loa!nR*1co.
}
Because there is no specific TS for the sequencers and considering
,
j
(1)
their unique interaction with numerous other systems and
j
equipment, and (2) the varying degrees in which related failures,
!
i
maintenance work, and surveillances can affect the sequencers'
j
associated functions, the inspection team concluded that additie.31
!
l
guidance for the operators is warranted.
Therefore, this issue
l
,
will be followed as an inspector followup item pending further
'
review and evaluation and is identified as
-
I
N-If
39- 6
IFI 50-424/90-M and 50-425/90-xm-94, "Iack of Operator Guidance
I
concerning the Leo Actions Applicable During ESFAS Sequencer
1
'
outages."
1
{
- .-
2:11211!ty -'
h-==~
v nine.1 r:eneratera
i
An allega
n indicated that VEGP counted the number of starts
failures
o
e
incorrectly
and
misrepresente
is
e
l
information know
in (1) a verbal presentation to
C,
(2)
a formal response to
Region II confirmation o
ction letter
l
(CAL), and (3) LER 90-00 ,
evision 0, issued
owing the March
j-
20, 1990, event involving fa
es of the
f1A.
In addition, it
j
was alleged that VEGP attempte
use the EDG reliability
issue with Revision 1, and delayed
-006, Revision 1, in order
.
j
to avoid drawing attention to
ese inco
et representations.
1-
i
Discussion
]
The
spection team reviewed the following:
i
i
LIMITED DISTRIBUTION - Not For Public Release
27
,
e
G
w--,
.
--w
vge
~
_
-,
-
,n-.
_ _ - . . . . - - - . - - . - . - - . .
.
. . . - . -
...
-
~
. - . . . - . - . . . . - -
.
1l.
.
i
LIMITED DISTRIEUTION - Nat For Public R31eC03
.
DRAFT - PREDECISIONAL INFORMATION
!,
,
1)
VEGP presentation in the Region II office ~ on April 9,
1990
concerning the site area emergency event of March 20, 19
.
his presentation is identified as Enclosure 2 to the Re
on
i
meeting summary letter of May 14, 1990.
/
1
~2)
VEG 1etter dated April 9,
1990, in response to the Region II
4
i
cont
ation of action letter (CAL) dated March 23,'1990.
}
}
!
j
3)
LER 90-006, issued April 19, 1990, to report the site area
emergen
event of March 20, 1990.
>
i
These documentsMnd the following procedures describe the EDG
operability.statu
and the licensee's program for recording EDG
!
start
information
and
the
surveillance
test
frequency
i
4
requirements:
\\
Procedure 550 8-C,
" Diesel Start.Ing"
l
?
'
Procedure
1314
-1,
"EDG
Operation
for
Maintenance
'
Troubleshooting
Maintenance Testing"
^
Procedure 14980-1,
EDG Operability Test"
i
\\/
e
l
The licensee indicated in a tran
arency used during the Region II
l
presentation that there were 18 s
cessful starts on EDG f1A and 19
i
successful starts on EDG $15
tyeen the loss-of-offsite-power
'
event (March 20,
1990) and the pXesentation to Region II of
-
April 9, 1990. The inspectiop' team r
iewed the EDG start logs and
j
the detailed EDG start records complet
during the performance of
i
Surveillance Procedures 13145-1 and 1498
-1.
The inspection team's
i
review of these records in'dicated that th
a were 31 EDG f1A and 29
EDG #1B attempted startpi
Two of the EDG
A and eight of the EDG
f1B starts involved pr#blems or failures.
EDG f1A there were a
'
i
total of 29 successful starts and on E
013 there were 21
i
problems or failurm/
successful starts.
However,
there were s veral intermittent
s during the EDG f18 start
tempts.
Although
there were 29
6
sequential starts
n EDG f1A,
the
inspection team,7 ccessful,
!
identified that there were on1
12 successful,
j
sequential staits of EDG $15 during this time peri
.
i
!
.a requires that each EDG be demonstrate
operable in
l
accordane
with the periodicity specified in TS Tabl
4 . 8-1 by
l
Verifyl
that the EDG starts and assumes rated fra
ency and
'
voltage in accordance with the EDG surveillance test
This
,
surve lance test required a minimum run time of 1 hou
at a
- .
.desi
ated load. The inspection team found that at the time
the
l
l
pre entation to the NRC, the operability test of the EDGs had een
s
cessfully demonstrated two times.
In addition, the EDGs
ad
l
LIMITED DISTRIBUTION - Not For Public Release
28
j-
i-
.
.
- . ,
n...
. , . . . .
-
n -.
. . . , - ,
,.
___
_ _ _
_ ..-_ _ _ . . _ _ _ _ _ _ _. _ __ _ _
_ _ __._.
_
._
i
..
.
LIMITED DISTRIBUTION - Not For Public Ralesso
.
DRAFT - PREDECISIONAL INFORMATION
i
uccessfully passed four operability tests before Unit i entere
j
e 2.
Therefore, the EDGs were reliable and operable before t e
i
j
presentation.
\\
/
-
The WRC Region II Office was
not verbally informed of the
l
j
incomp'lete information regarding the number of EDG starts until
'
1
June 11
1990 (approximately 2 months after.the presentation).
.
j
Although
evision 1 of LER 90-006, dated June 29, 1990, correctly
!
)
identifiedsthe number of sequential, successful EDG starts from the
i
j
and of the'saintenance test program
(i.e.,
the first successful
!
operability
st per TS 4. s . l .1. 2 a ) until the issuance of LER 90-
i
006, Revision
dated April 19, 1990, this revision (June 29,
,
j
1990) did not address the number of EDG starts that should have
been cited in th presentation, in the VEGP letter in response to
the CAL, and in
R 90-006, Revision
O.
The correct number of
,
j
sequential, ' success ul starts for EDG #18 was 12 and not 19 as
!
indicated in the pres tation. Therefore, the NRC was not informed
l
of the correct informa ion in a timely manner.
1
The information presente
to the NRC did not coopletely describe
.
the problems and failures k at occurred with EDG $18. However, the
i
testimony indicates that t
general manager's intention was to
'
i
demonstrate that the problem
involving the immediate trip of EDGs
identified during and follow
gfthe March 20,
1990 event were
corrected prior to Unit 1 start
Therefore, a compliation of the
.-
total number of successful sta' s
(i.e.,
a start that did not
immediatelytrip)wasanimp/
ortan
factor in his presentation.
s
i
l
The testimony also indica
d that
e unit superinten: lent (Us)
i
researched the EDG starti
history fo the NRC presentation based
-
on a request from the ge
ral manager.
e general manager did not
ask the US to prepare a complete descri
ion of the EDG starting
i
history. specifica11 ' the general manage requested a summary of
l
only the successfu
starts--the informati
concerning the EDG
j
problems and fallu s was not requested.
In ddition, the Us used
j
the unit reactor
rator logs instead of the E
operating logs to
compile the EDG
tarting history.
The reactor perator logs did
!
not contain a
etailed description of problems
failures which
!
occurred dur g the EDG starts.
The US did not
ceive specific
j
guidance co erning the type.of EDG starts that he w
requested to
l
summarise.
In addition, the testimony indicated that the original
assumptigns and EDG $1B start information used in the
esentation
,
were alp 6 used in the VEGP response to the CAL, and in
R 90-006
issuedApril 19, 1990.
i
,
.
The [nspection team's review of ' the Unit 1 EDG's reliabil
f
and
o
rability status between March 21 and June 14, 1990, raise
the
11owing additional concern.
The review was performed to ve
fy
l
LIMITED DISTRIBUTION - Not For Public Release
29
.
t
'
4
!
'
.
,
!
,.
. ,
, . . . , . . , ,
, , _ .
._.
_ . _ _
. - - .
_
. _ _ _ .
- --
_ _ _
,
,.
,
LIMITED DISTRIBUTION - Not For Public R31ocS3
DRAFT - PREDECISIONAL INFORMATION
t at all EDG failures were identified and classified as eit
r
va id or non-valid and were reported to the NRC as required b TS 4.8. .1.3 and TS 6.8.2.
The inspection team discovered tha
the
foll
ing f ailures during starts of EDG f1B had not been clas ified
as val d or non-valid and, consequently, had not been repofted to
the NRC ursuant to TS 4.8.1.1.3 and TS 6.8.2.
EDG S art
Date
Remarks
/
1-90-13
3/22/90
trfp,
high-
temperature
lube
oil.
Ma i n 't e na nce
troubleshooting test.
/
1-90-134
3/23/90
EDG / trip,
low
jacket
water
pressure.
M ,4
i nt a nance
troubleshooting test.
2
.
1-90-136
3 24/90
EDG intentionally stopped
due to alarmed condition,
high
jacket
water
temperature.
Maintenance
troubleshooting test.
1-90-157
5/23/ 0
trip,
high
jacket
water
temperature
M a i nt e na nce
troubleshooting test.
i
<
1-90-160
5/23/90
END G
trip,
1ow
4
tutbocharger
-161
o i'
pressure.
Main
nance
-162
troub e. shooting test.
\\
'
'
1-90-164
5/23/90
trip
high
jacket
'
water
-163
temperature.
Maintenance
troubleshoot
g test.
These in
.ction findings were discussed with the e
ineering
support
anager who agreed that these types of failures
ave not
'
been
ported.
The licensee committed to have all E
start
recor s reviewed for any unreported failures.
,
Th
inspection team also four.. that a violation -as previou ly
i entified for the failure to report all EDG failures in Inspecti
LIMITED DISTRIBUTION - Not For Public Release
30
.
e
l
l
- - - -
--- . -
- -
-
. ~ - - .
- . - . - - -_----..- _- -. - _ - .
- -.. -- - - - . - -
.
.
~
LIMITED DISTRIBUTION - Not For Public R310000
]
DRAFT - PREDECISIONAL INFORMATION
Re
rt 50-424/87-57 dated November 1987.
Although the failur
to
,
repo
all EDG failures is a violation of TS 3.8.1.1.3
d TS
,
6.8.2,
the inspection team concluded that the failure
s the
'
result
inadequate implementation of corrective a
ions to
j
prevent re urrence of a violation and, as such, is a vjdlation of
l
10 CFR 50 Ap ndix 8, Criterion XVI, " Corrective Actiop," and will
be followed a
-
VIO 50-424/90-xx-
" Failure to Determine and Implement Adequate
,
j
Corrective Actions.
,
,
/
j
Conclusion
/
1
/
i
The. allegation that VEGP i
orrectly counted the number of starts
and feilures of the EDGs a
knowingly misrepresented the EDG
'
reliability
in
order
to
s1 cad
the
NRC
was
partially
.
.
substantiated.
On the basis of
u sworn testimony and its review
j
j
of EDG records, the. inspection te
concluded that the Region II
1
presentation was not intended to r
resent a specific number of
,
j
successful valid tests as specified in
G 1.108 and TS 4. 8.1.1.2a,
i
but rather to describe the EDG maintenan
test program and the EDG
!
reliability status.
Nevertheless, the i
ction team concluded
,
i
that the NRC was not informed of the incor et information until
the NRC asked for it dh[ ring the inspection.
e lack of specific
guidance concerning
he EDG information desi
d,
coupled with
inadequate researc
of the EDG starting histo
resulted in
1
,
providing incomp te and therefore inaccurate infotsation to the
]
NEC.
The CAL r ponse and LER 90-006 were also inco
ct because
they were bas
on the IDG start information that was c
iled for
!
the VEGP pr antation in the Region II Office. The inspec
on teaa
!
concluded
at the failure to provide accurate information
o the
]
NRC was a violation of 10 CFR 50.9 requirements and wil
be
l
follow
as:
.
l
VI
50-424/0-xx-05; 50-425/90-xx-05, " Failure to provide Accurate
ornation to the NRC."
r
,
7 6 y Air Quality of Emeraency Diesel Generator Startina Air System
\\
,
An allegation indicated that VEGP had no basis for its conclusions
i
regarding the air quality of the EDG starting air system and
misrepresented the air quality in the licensee's written response
,
to the CAL.
I
f
Discussion
i
i
The ir. pection team reviewed the maintenance records and deficiency
cards associated with Unit 1 EDG starting air system.
The team
i
!
LIMITED DISTRIBUTION - Not For Public Release
i
31
'
'
!.
!
t
'
.
'
,
9
I
e
-
-
.
.
.
, - ,
-
-
-
.
-
-. --
.
. ..
--
-
-
-.
. _ ._
._.__ --
- - -
.
q.-
-
,
4
} .
LIMITED DISTRIBUTION - Not For Public Release
DRAFT - PREDECISIONAL INFORMATION
,
was established when preoperational tests were ini
,
4
on Unit 1 in November 1986.
t
but' not on a scheduled frequency. Dewpoint measurements w
this date,
'
'
part of 1988,
During the latter
!
established to measure the EDG starting air system dewpoi
i
{
current PM progran required checking the dewpoint monthly, cleanin
!
The
the air dr
!
addition, yer condensing units, and cleaning the fan motors.
i
'
operating Procedure 11882-1,
"Outside Area Rounds,"
i
In
dryers be blown down on a daily basis untilrequired that the E
i
i
)
i
i
noisture.
they were free of
The inspection team verified that the plant equipment
,
operators blev
down the air systems on each shift during the
i
!
performance of their rounds.
!
A review of the Unit 1 EDG maintenance history records indicat d
i
that the majority of the devpoint measurements taken were withi
e
specifications.
i
.
There were instances,
n
i
asasurements were above specifications.however, when the dewpoint
j
primarily attributed to problems with (1)
These conditions were
i
instruments,
(2) system air dryers beingthe dewpoint measuring
l
extended pwriods of time, and
out of service for
system following maintenance. (3) repressurizing the EDG air start
i
The inspection team reviewed maintenance records associated with
s
internal inspection of the EDG air start system air receiveran
micron control _ air system filter inspection and replacement
,
5-
the replacement of the dowpoint measuring instrument with an EG6
, and
analyzer.
Following the loss of offsite power event of March 20
i
G
1990, the control air system instrument lines were disconnected f
maintenance troubleshooting and functional tests of Calcon sensors
,-
or
The system engineers associated with this work stated that no
evidence of internal noisture or corrosion was noted during
.
i
inspection and calibration of the calcon sensors or the cortrol
system instrument lines when this equipment was disconnected for
air
.
maintenance troubleshooting and testing.
!
j
Conclusion
'
!.
-
The inspection team concluded that the licensee did have an
adequate basis to assess the quality of the EDG starting air
,
{
'
system.
inspection of EDG air start system components for degr
1
addition,
the
PM program dewpoint readings have shown more
a
on.
In
The allegation that VEGP did not have a basis for th
i
er.
concerning
air
start
system
quality
was
not
-M4y
i
-4.i.uil-i A
C #id *4 C D
a ements
I
y
LIMITED DISTRIBUTION - Not For Public Release
'
'
32
um * A L m. eta & Guy as@v
yQWidLC. INhgebm.
.
.
i
!
- , . . _ _
-
_
.
. . .
_
.
- , _
-
. - _ -
-.
. - - - - .
- -
- - - _ - - - . . . . _ _ . - - . - - -
.- -
!
c
!
j.
-
t
- .
i
j
LIMITED DISTRIBUTION - Not For Public Release
'
DRAFT - PREDECISIONAL INFORMATION
M
y Reportability of Previous System Outages
l
f
\\<
!
An allegation indicated that VEGP failed to immediately notify the
>
{
NRC as required by 10 CFR 50.72 when VEGP identified that both
j
trains of the containment fan coolers (CFCs) had been previously
i
j
inoperable at the same time on Unit 1.
.
I
Discussion
i
i.
The inspection team's review of plant records indicated that this
!
I
!
condition occurred when EDG f1A was declared inoperable when tape
(used when the EDG was being painted) was found on the EDG fuel
j
rack.
The tape kept the fuel injector piston from moving and
i
injecting fuel into the EDG.
With EDG f1A inoperable,
the
.
equipment associated with the Train A was also inoperable.
In the
process of investigating the installation of the tape, VEGP
!
identified that this condition existed during a period when the
i;
Train B containment fan coolers were also in a degraded condition
j
for maintenance.
i
'
During the performance of Surveillance. Procedure 14623-1, Train B
i
containment fan cooler (CFC) 1-1501-A7-003 failed to start in slow
!
1
speed.
140 1-90-560 was initiated at 0115 hours0.00133 days <br />0.0319 hours <br />1.901455e-4 weeks <br />4.37575e-5 months <br /> on June 19, 1990,
J
and maintenance on the CFC was initiated.
The CFC was returned to
j
operable status on June 19,1990, at 1415 hours0.0164 days <br />0.393 hours <br />0.00234 weeks <br />5.384075e-4 months <br />.
Approximately 9
hours later [on June 19,1990, at 2359 (Lco 1-90-562)), EDG f1A was
i
determined to be inoperable because the tape had been installed on
i-
the fuel rack.
On July 17, 1990, VEGP issued LER 90-014 to
j
identify the previously unrecognized violation of the 140 in
accordance with 10 CFR 50.73.
'
Conclusion
,
!
Based upon the fact that VEGP did not become aware that both trains
,
of CFCs were simultaneously inoperable until after the Train B CFC
!
fan had been returned to service, the immediate notification
j
requirements of 10 CFR 50.72 were not applicable.
The allegation
that VEGP failed to immediately notify the NRC upon discovery of
the previously degraded c
of the CFCs was not .Se44y
,
e , - ,ondition
>
.
j
g.1 W Intimidation of Plant Review Board
(PRB) Members
i
i
An allegation indicated that Plant Review Board (PRB) members were
allegedl
f
meeting.y intimidated and pressured by the general manager in a PRB
j
The meeting occurred in February 1990, to determine the
}
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DRAFT - PREDECISIONAL INFORMATION
acceptability of the safety analysis for the installation of the
FAVA microfiltration system.
Discussion
T.i
j
k
As discussed in Section ht" of this inspection report, several
,
!
safety evaluations were performed for the installation of a
'
temporary modification which installed the FAVA microfiltration
i
system.
Discussions with PRB members indicated that during the
t
review of these safety evaluations,
various PRB members had
1
expressed
reservations
on
several
occasions
concerning
the
4
acceptability of the installation of the FAVA system.
!
.'
Despite these reservations, the inspection team's review of the PRB
Meeting minutes
associated
with
this
j
identified few instances of the PRB members documenting their
i
dissenting opinions.
Specifically,
PRB meeting 90-15
(dated
'
February 8, 1990) documented one PRB member's negative vote and
i
dissenting opinions regarding the acceptability of exempting the
from
regu'.atory
requirements
and
the
adequacy of the system's safety evaluation.
PRS Meeting 90-28
,
(dated March
1,
1990)
indicated that information and issues
.
regarding the FAVA system's safety analysis were presented to the
j
PRB and that the general manager solicited written comments and
!
questions from other members for resolution.
The only other
l
example was in PRB meeting 90-32 (dated March
6,
1990) which
!-
identified a dissenting opinion related to the acceptability of
j
votina on the FAVA system installation when the PRB member who
raised the initial questions and concerns on the operation of the
i
FAVA system was not present.
!
Discussions with the PRB members indicated that during the various
PRB meetings concerning the installation of the FAVA system, the
i
PRB members felt intimidated and pressured by the presence of the
'
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general manager at the PRB meeting.
The sworn testimony confirmed
that on one occasion an alternate voting member felt intimidated
4
and feared retribution or retaliation because the general manager
i
j
was present at the meeting and the PRB member knew the general
1
j.
manager wanted to have the
temporary modification approved.
j
However, the testimony also indicated that the.PRB member did not
'
alter his vote and felt comfortable with how he had voted.
In
a
l
addition, the PRB member was not aware of any occasions on which he
or any other PRB member had succumbed to intimidation or feared
i
!
retribution.
!
'
The incpection team verified that the general manager was informed
following this meeting that several PRB members viewed his presence
i
as intimidating.
As a result, on March
1,
1990, the general
,
!
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manager set with all PRB members to reiterate the member's duties
and responsibilities.
He specifically told the members that his
presence at PRB meetings must not
influence them and that
!
alternates should be selected who would feel comfortable with this
i
responsibility.
He
also
addressed
the
difference
between
professional differences of opinion and safety or quality concerns,
and their respective methods for resolution.
conclusion
,
The inspection team concluded that in on* case a PR
felt intimidated and feared retribution because the general manager
l
was present at the PRB meeting.
However, this member 6ala nor W
change his vote in response to this pressure and the general
manager met with the PRB to allay fears.
Based on the testimony,
i
the inspection team concluded that retribution did not occur.
Nevertheless, this confirmed event and the absence of dissenting
'
opinions in the PRB meeting minutes indicate that there was a
'
potential for an adverse affect on open discussions at the meeting,
t
The licensee needs to ensure that PRB members
freel
express their technical opinions and safety concerns.y and openly
K Personnel Accountability
As a result of several comments and questions by the licenced
operators to the inspection team, the team reviewed the method used
to rate the
supervisors. performance of the shift superintendents and unit shift
Discussion
The o
rations manager stated that the shift superintendents (SSs)
"
e SSs re
ed to
su
int ndent
s
and
a
i
US personally prepared the performance appraisals of the 8 s.
The personnel accountability system, first used in 1989, was a pay-
i
for-performance methodology. Annual pay increases and e percentage
of the Operations Department bonus were dependent on their ratings
i
in accountability categories.
subdivided into performance categories.Each accountability category was
,
.
Most of the performance
i
categories vern based upon group performance.
Once these are
i
'
eliminated,
any differential
in pay will
result from eight
performance categories. Implementation of the plan in 1989 could
t
result in up to an $8,000-a-year difference 'n bcnus pay to a shift
i
superintendent.
The performance categories and their relative
weights are:
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- - -
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Personnel safety
4.1%
.
Regulatory compliance
10.2%
.
.
}
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ESFAS actuation
12.2%
!
10.2%
'
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MWO performance
4.1%
Special projects
a.2%
.
'
'
Personnel development
30.6%
=
l
Training
.
20.4%
i
Therefore, 51 percent will be associated with personnel development
,
{
and training and 32.6 percent will be associated with the number of
]
LERs, and violations (i.e. , regulatory compliance (10.2 percent),
.
ESFAS actuation (12.2 percent) and reactor trips (10.2 percent)].
'
Conclusion
'
t
The
inspection
team
concluded
that
there
was
a
potential
disincentive for identifying items which may result in LERs or
,
'
violations.
In addition, the inspection team concluded that the
'
operations manager provided incorrect or inadequately researched
!
j
information to the inspection team.
The inaccurate information
)
i
concerned whether the operations manager personally performed the
performance appraisals of shift superintendents.
The information
i
a
-was not very important because the inspection team did not use the
3
information as the basis for a significant inspection finding.
{
j
inspection team concluded that this
The
failure to provide accurate
]
-
information was an example of a violation of the 10CFR 50.9
i
requirements to provide accurate information to the NRC and will be
{
followed as:
14-1L-
Ig-12.
'
VIO 50-424/90-aoeHPJ; 50-425/90.xx-65, " Failure to Provide Accurate
,
Information to the NRC."
'
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3.0
EXIT INTERVIEWS
1
The inspection scope and findings were summarized on August
'
1990, with those persons indicated in Appendix 2.
17,
i
The inspection
team described the areas inspected and discussed in detail the
inspection results.
The
licensee
made
numerous
dissenting
comments.
materials provided to or reviewedThe licensee did not identify as proprietary any o
,
i
i
inspection.
by the inspector during this
]-
,
.
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APPENDIX 1
LIST OF TRANSCRIBED INTERVIEWS
DATE
TIME
PERSON
,
8/14/90
904 hours0.0105 days <br />0.251 hours <br />0.00149 weeks <br />3.43972e-4 months <br />
George Bockhold
911 hours0.0105 days <br />0.253 hours <br />0.00151 weeks <br />3.466355e-4 months <br />
Jim Swartzwelder
1023 hours0.0118 days <br />0.284 hours <br />0.00169 weeks <br />3.892515e-4 months <br />
Harvey Handfinger
1026 hours0.0119 days <br />0.285 hours <br />0.0017 weeks <br />3.90393e-4 months <br />
Bill Diehl
1109 hours0.0128 days <br />0.308 hours <br />0.00183 weeks <br />4.219745e-4 months <br />
Mike Horton
1335 hours0.0155 days <br />0.371 hours <br />0.00221 weeks <br />5.079675e-4 months <br />
Mike Chance
1136 hours0.0131 days <br />0.316 hours <br />0.00188 weeks <br />4.32248e-4 months <br />
Jimmy Paul cash
1338 hours0.0155 days <br />0.372 hours <br />0.00221 weeks <br />5.09109e-4 months <br />
Dudley Carter
1529 hours0.0177 days <br />0.425 hours <br />0.00253 weeks <br />5.817845e-4 months <br />
Bruce Kaplan
1625 hours0.0188 days <br />0.451 hours <br />0.00269 weeks <br />6.183125e-4 months <br />
Greg Lee
1800 hours0.0208 days <br />0.5 hours <br />0.00298 weeks <br />6.849e-4 months <br />
Jeff Gasser
8/15/90
906 hours0.0105 days <br />0.252 hours <br />0.0015 weeks <br />3.44733e-4 months <br />
Allen Mosbaugh
937 hours0.0108 days <br />0.26 hours <br />0.00155 weeks <br />3.565285e-4 months <br />
Ernie Thornton
1009 hours0.0117 days <br />0.28 hours <br />0.00167 weeks <br />3.839245e-4 months <br />
John Gwin
1048 hours0.0121 days <br />0.291 hours <br />0.00173 weeks <br />3.98764e-4 months <br />
Steve Waldrup
1335 hours0.0155 days <br />0.371 hours <br />0.00221 weeks <br />5.079675e-4 months <br />
Jerry Bowden
1452 hours0.0168 days <br />0.403 hours <br />0.0024 weeks <br />5.52486e-4 months <br />
John williams
1637 hours0.0189 days <br />0.455 hours <br />0.00271 weeks <br />6.228785e-4 months <br />
Carolyn Tynan
1730 hours0.02 days <br />0.481 hours <br />0.00286 weeks <br />6.58265e-4 months <br />
John Williams
!
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9
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APPENDIX 2
PERSONS CONTACTED
Licensee Employees
- J. Aufdenkampe, Manager Technical Support
- G.
Bockhold, Jr. , General Manager Nuclear Plant
- D. Carter, Shift Superintendent
J. Bowden, Work Planning
,
J. Cash, Unit Superintendent
M. Chance, Senior Engineer, Engineering Support
,
- S. Chesnut, Technical Support
i
C. Coursey, Mair.cenance Superintendent
l
W. Diehl, Shif t Supervisor, Operations
,
- G. Frederick, Safety Audit and Engineering Group Supervisor
1
J. Gasser, Shift Superintendent, Operations
- L. Glenn, Manager. - Corporate Concerns
- D. Gustafson, Maintenance Engineering Supervisor
i
J. Gwin, Corporate Systen Engineer
- H. Handfinger, Manager Maintenance
- K. Holmes, Manager Training and Emergency Preparedness
!
- M. Horton, Manager Engineering Support
.
,
B. Kaplan, Senior Engineer, Engineering Support
G. Lee, Plant Engineering Supervisor, Operations
- R. LeGrand, Manager Health Physics and Chemistry
W. Lyons, Quality Concerns Coordinator
- G. McCarley, Independent safety Engineering Group Supervisor
- C. McCoy, Vice-President, Georgia Power Company
- R. Mcdonald, Executive Vice-President, Georgia Power Company
- D. Moncus, Outage and Planning
- A. Mosbaugh, VEGP Staff
'
R. Odom, Nuclear Safety and Compliance Manager
- A. Rickman, Senior Engineer - Nuclear Safety and Compliance
i
- L. Russell, Independent safety Engineering Group, SONOPCO
- M. Shelbani, Senior Engineer
!
- C. Stinespring, Manager Plant Administration
- S. Swanson, Outage and Planning Supervisor
- J. Swartzwelder, Manager Operations
-
E. Thorton, Shif t Supervisor, Operations
I
- E. Toupin, Oglethorpe Power Corporation
.
C. Tynan, PRB Secretary
i
S. Waldrup, Planning and Scheduling Supervisor
J. Williams, Shift Superintendent, Operations
,
Attended exit interview, August 16, 1990.
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- _ . - - - . _ - -
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APPENDIX 2
PERSONS CONTACTED (continued)
NRC Employees Who Attended Exit Interview
!
R. Aiello, Resident Inspector - Vogtle
-
B. Bonser, Senior Resident Inspector - Vogtle
M. Branch, Senior Resident Inspector - Watts Bar
R. Carroll, Project Engineer - RIIK. Brockman, Chief, Reacto
N. Huneauller, Reactor Engineer - NRRL. Carner, Senior R
i
0. Matthews, Project Director - NRR
>
J. Milhoan, Deputy Regional Administrator - RII
R. Starkey, Resident Inspector - VogtleL. Reyes, Directo
P. Taylor, Reactor Inspector - RII
M. Thomas, Reactor Inspector - RII
C. VanDenburgh, Section Chief - NRR
J. Wilcox, Operation Engineer - NRR
,
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APPENDIX 3
LIST OF ACRONYMS
i
Abnormal Operating Procedure
ARB.
Alternate radwaste building
ASME'
American Society of Mechanical Engineers
Confirmation of action letter
i
Containment Fan Cooler
j
CFR
Code of Federal Regulations
containment isolation valve
Deficiency card
Division of Reactor Projects
i
Electric Power Research Institute
'
Engineered safety features
Engineered safety features actuation system
TSAR
Final Safety Analysis Report
NUT
Holdup tank
Instrumentation and controls
IFI
Inspector follovup iten
Inservice test
kV
Kilovolt
LCO
Limiting condition for operation
LER
Licensee Event Report
NWO
Maintenance work order
NRC
Nuclear Regulatory Commission
Nuclear Reactor Regulation
Nuclear service cooling water
Nuclear steam supply system
Office of Investigations
Preventative maintenance
Plant Review Board
psig
Pounds per square inch gauge
Polyvinyl chloride
Quality Assurance
RII
Region II Office
l
REA
Request for engineering assistance
Regulatory Guide
,
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l
Safety Evaluation Report
j
safety injection
i
SONOPCO
Southern Nuclear Operating Company
Source range monitor
shift superintendent
.
'
Shift support supervisor
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APPENDIX 3
'
LIST OF ACRONYMS (continued)
Surveillance task sheet
Temporary change to procedure
TS
Technical Specification
USS
Unit shift superintendent
Vogtle Electric Generati!.g Plant
Violation
,
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