ML13065A049: Difference between revisions

From kanterella
Jump to navigation Jump to search
(Created page by program invented by StriderTol)
(Created page by program invented by StriderTol)
 
Line 17: Line 17:


=Text=
=Text=
{{#Wiki_filter:August 3, 2012
{{#Wiki_filter:UNITED STATES
 
                                  NUCLEAR REGULATORY COMMISSION
                                                    REGION I V
Matthew W. Sunseri, President and  
                                                1600 EAST LAMAR BLVD
  Chief Executive Officer
                                          ARLINGTON, TEXAS 76011-4511
Wolf Creek Nuclear Operating  
                                            August 3, 2012
Corporation
Matthew W. Sunseri, President and
P. O. Box  
  Chief Executive Officer
411 Burlington, KS
Wolf Creek Nuclear Operating Corporation
  66839
P. O. Box 411
SUBJECT: WOLF CREEK GENERATING STATION  
Burlington, KS 66839
- INTEGRATED INSPECTION REPORT 05000482/201200
SUBJECT:       WOLF CREEK GENERATING STATION - INTEGRATED INSPECTION
                REPORT 05000482/2012003
Dear Mr. Sunseri:
Dear Mr. Sunseri:
  On June 29, 2012, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Wolf Creek facility. The enclosed inspection report documents the inspection results which were discussed on July 18, 2012, with Mr. Richard Clemens
On June 29, 2012, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at
and other members of your staff.
your Wolf Creek facility. The enclosed inspection report documents the inspection results which
  The inspections examined activities conducted under your license as they relate to safety and compliance with the Commission
were discussed on July 18, 2012, with Mr. Richard Clemens and other members of your staff.
's rules and regulations and with the conditions of your license. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.
The inspections examined activities conducted under your license as they relate to safety and
  One NRC identified
compliance with the Commissions rules and regulations and with the conditions of your license.
finding and one self-revealing finding of very low safety significance (Green) were identified during this inspection.
The inspectors reviewed selected procedures and records, observed activities, and interviewed
  Both of these findings were determined to involve violations of NRC requirements.
personnel.
  Further, a licensee
One NRC identified finding and one self-revealing finding of very low safety significance (Green)
-identified violation which was determined to be of very low safety significance is listed in this report. The NRC is treating these violation s as non-cited violation
were identified during this inspection. Both of these findings were determined to involve
s (NCV s) consistent with Section 2.3.2 of the Enforcement Policy.
violations of NRC requirements. Further, a licensee-identified violation which was determined to
  If you contest these non
be of very low safety significance is listed in this report. The NRC is treating these violations as
-cited violations , you should provide a response within 30
non-cited violations (NCVs) consistent with Section 2.3.2 of the Enforcement Policy.
days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington DC 20555
If you contest these non-cited violations, you should provide a response within 30 days of the
-0001; with copies to the Regional Administrator, Region IV; the Director, Office of Enforcement, United States Nuclear  
date of this inspection report, with the basis for your denial, to the Nuclear Regulatory
Regulatory Commission, Washington, DC 20555
Commission, ATTN: Document Control Desk, Washington DC 20555-0001; with copies to the
-0001; and the NRC Resident Inspector at
Regional Administrator, Region IV; the Director, Office of Enforcement, United States Nuclear
the Wolf Creek Generating Station
Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at the
If you disagree with a crosscutting aspect assignment in this report, you should provide a  
Wolf Creek Generating Station.
response within 30
If you disagree with a crosscutting aspect assignment in this report, you should provide a
days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region IV; and the NRC Resident Inspector at the Wolf Creek Generating Station
response within 30 days of the date of this inspection report, with the basis for your
.
disagreement, to the Regional Administrator, Region IV; and the NRC Resident Inspector at the
In accordance with 10
Wolf Creek Generating Station.
CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's Agencywide
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its
Document Access and Management System (ADAMS). ADAMS is  
enclosure, and your response (if any) will be available electronically for public inspection in the
U N I T E D S T A T E S N U C L E A R R E G U L A T O R Y C O M M I S S I O N R E G I O N I V1600 EAST LAMAR BLVD
NRC Public Document Room or from the Publicly Available Records (PARS) component of
A R L I N G T O N , T E X A S 7 6 0 1 1-4511 
NRC's Agencywide Document Access and Management System (ADAMS). ADAMS is
M. Suneri - 2 -  accessible from the NRC Web site at http://www.nrc.gov/reading
 
-rm/adams.html
M. Suneri                                    -2-
(the Public Electronic Reading Room).
accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public
  Sincerely,
Electronic Reading Room).
/RA/
                                            Sincerely,
Neil O'Keefe, Chief
                                            /RA/
Project Branch B
                                            Neil OKeefe, Chief
Division of Reactor Projects
                                            Project Branch B
  Docket No.: 05000482  
                                            Division of Reactor Projects
License No: NPF
Docket No.: 05000482
-42   Enclosure: Inspection Report 05000482/2012003  
License No: NPF-42
w/ Attachment: Supplemental Information
Enclosure: Inspection Report 05000482/2012003
  cc w/ encl: Electronic Distribution
          w/ Attachment: Supplemental Information
   
cc w/ encl: Electronic Distribution
M. Suneri - 3 -  Electronic distribution by RIV:  
 
  Regional Administrator (Elmo.Collins@nrc.gov)  
M. Suneri                                     -3-
   
  Electronic distribution by RIV:
Deputy Regional Administrator (Art.Howell@nrc.gov)  
  Regional Administrator (Elmo.Collins@nrc.gov)
  DRP Director (Kriss.Kennedy@nrc.gov)  
  Deputy Regional Administrator (Art.Howell@nrc.gov)
  Acting DRP Deputy Director (Allen.Howe@nrc.gov)  
  DRP Director (Kriss.Kennedy@nrc.gov)
  Acting DRS Director (Tom.Blount @nrc.gov)  Acting DRS Deputy Director (Patrick.Louden@nrc.gov)  
  Acting DRP Deputy Director (Allen.Howe@nrc.gov)
  Senior Resident Inspector (Chris.Long@nrc.gov)  
  Acting DRS Director (Tom.Blount @nrc.gov)
  Resident Inspector (Charles.Peabody@nrc.gov)  
  Acting DRS Deputy Director (Patrick.Louden@nrc.gov)
  WC Administrative Assistant (Shirley.Allen@nrc.gov)  
  Senior Resident Inspector (Chris.Long@nrc.gov)
  Branch Chief, DRP/B (Neil.OKeefe@nrc.gov)  
  Resident Inspector (Charles.Peabody@nrc.gov)
  Senior Project Engineer, DRP/B (Leonard.Willoughby@nrc.gov)  
  WC Administrative Assistant (Shirley.Allen@nrc.gov)
  Project Engineer, DRP/B (Nestor.Makris@nrc.gov)  
  Branch Chief, DRP/B (Neil.OKeefe@nrc.gov)
  Public Affairs Officer (Victor.Dricks@nrc.gov)  
  Senior Project Engineer, DRP/B (Leonard.Willoughby@nrc.gov)
  Public Affairs Officer (Lara.Uselding@nrc.gov)  
  Project Engineer, DRP/B (Nestor.Makris@nrc.gov)
  Project Manager (Terry.Beltz@nrc.gov)  
  Public Affairs Officer (Victor.Dricks@nrc.gov)
  Acting Branch Chief, DRS/TSB (Dale.Powers@nrc.gov)  
  Public Affairs Officer (Lara.Uselding@nrc.gov)
  RITS Coordinator (Marisa.Herrera@nrc.gov)  
  Project Manager (Terry.Beltz@nrc.gov)
  Regional Counsel (Karla.Fuller@nrc.gov)  
  Acting Branch Chief, DRS/TSB (Dale.Powers@nrc.gov)
  Congressional Affairs Officer (Jenny.Weil@nrc.gov)  
  RITS Coordinator (Marisa.Herrera@nrc.gov)
  OEMail Resource  
  Regional Counsel (Karla.Fuller@nrc.gov)
  DRS/TSB STA (Dale.Powers@nrc.gov)  
  Congressional Affairs Officer (Jenny.Weil@nrc.gov)
  Executive Technical Assistant  
  OEMail Resource
(Silas.Kennedy@nrc.gov)   R:\_REACTORS\_WC\2012\2012003.docx
  DRS/TSB STA (Dale.Powers@nrc.gov)
SUNSI Rev Compl.
  Executive Technical Assistant (Silas.Kennedy@nrc.gov)
Yes  No ADAMS Yes  No Reviewer Initials
R:\_REACTORS\_WC\2012\2012003.docx
NFO Publicly Avail.
SUNSI Rev Compl. Yes  No ADAMS                   Yes  No   Reviewer Initials   NFO
Yes  No Sensitive Yes  No Sens. Type Initials
Publicly Avail.         Yes  No Sensitive         Yes  No   Sens. Type Initials NFO
NFO SRI:DRP/B RI:DRP/B SPE:DRP/B C:DRS/EB1 C:DRS/EB2 C:DRS/OB CLong CPeabody LWilloughby
SRI:DRP/B         RI:DRP/B         SPE:DRP/B   C:DRS/EB1     C:DRS/EB2       C:DRS/OB
  TFarnholtz
CLong             CPeabody         LWilloughby  TFarnholtz   GMiller         MHaire
GMiller MHaire /NFO via E/
/NFO via E/       /NFO via E/       /RA via E/   /RA/         /RA/             /NFO via T/
/NFO via E/
7/20/12           7/20/12           8/9/12       7/31/12       7/31/12         8/1/12
/RA via E/
C:DRS/PSB1 C:DRS/PSB2 AC:DRS/TSB                 BC:DRP/B
  /RA/ /RA/ /NFO via T/
MHay             JDrake           RKellar     NOKeefe
7/20/12 7/20/12 8/9/12 7/31/12 7/31/12 8/1/12 C:DRS/PSB1
/RA/             /RA/             DPowers for  /RA/
C:DRS/PSB2
8/1/12           8/1/12           8/1/12       8/3/12
AC:DRS/TSB
OFFICIAL RECORD COPY                               T=Telephone     E=Email         F=Fax
BC:DRP/B   MHay JDrake RKellar NO'Keefe  /RA/ /RA/ DPowers for
 
  /RA/   8/1/12 8/1/12 8/1/12 8/3/12   OFFICIAL RECORD COPY                                   T=Telephone           E=Email           F=Fax
            U.S. NUCLEAR REGULATORY COMMISSION
   
                              REGION IV
  U.S. NUCLEAR REGULATORY COMMISSION
Docket:     05000482
REGION IV Docket: 05000 482 License: NPF-042 Report: 05000 482/20 12 0 0 3 Licensee: Wolf Creek Nuclear Operating Corporation
License:   NPF-042
Facility: Wolf Creek Generating Station
Report:     05000482/2012003
Location: 1550 Oxen Lane  
Licensee:   Wolf Creek Nuclear Operating Corporation
NE, Burlington, Kansas
Facility:   Wolf Creek Generating Station
Dates: March 31 through June 29, 2012 Inspectors:
Location:   1550 Oxen Lane NE, Burlington, Kansas
C. Long, Senior Resident Inspector
Dates:     March 31 through June 29, 2012
C. Peabody, Resident Inspector
Inspectors: C. Long, Senior Resident Inspector
N. Makris, Project Engineer
            C. Peabody, Resident Inspector
C. Alldredge, Health Physicist
            N. Makris, Project Engineer
N. Greene , PhD, Health Physicist
            C. Alldredge, Health Physicist
L. Carson II, Senior Health Physicist
            N. Greene, PhD, Health Physicist
J. O'Donnell, Health Physicist
            L. Carson II, Senior Health Physicist
L. Ricketson, P.E., Senior Health Physicist
            J. ODonnell, Health Physicist
  Approved By: Neil O'Keefe, Chief, Project Branch  
            L. Ricketson, P.E., Senior Health Physicist
Division of Reactor Projects
Approved   Neil OKeefe, Chief, Project Branch B
   
    By:      Division of Reactor Projects
  - 2 - Enclosure SUMMARY OF FINDINGS
 
  IR 05000 482/2012003; 03/31/2012 - 06/29/2012
                                    SUMMARY OF FINDINGS
; Wolf Creek Generation Station, Integrated Resident and Regional Report;
IR 05000482/2012003; 03/31/2012 - 06/29/2012; Wolf Creek Generation Station, Integrated
Flood Protection Measures, Plant Modifications.
Resident and Regional Report; Flood Protection Measures, Plant Modifications.
  The report covered a 3
The report covered a 3-month period of inspection by resident inspectors and an announced
-month period of inspection by resident inspectors and an announced baseline inspection by region
baseline inspection by region-based inspectors. Two Green noncited violations of significance
-based inspectors. Two Green noncited violations of significance were identified. The significance of most findings is indicated by their color (Green, White, Yellow, or Red) using Inspection Manual Chapter
were identified. The significance of most findings is indicated by their color (Green, White,
0609, "Significance Determination Process.The crosscutting aspect is determined using Inspection Manual Chapter 0310, "Components  
Yellow, or Red) using Inspection Manual Chapter 0609, Significance Determination Process.
Within the Cross Cutting Areas.Findings for which the significance determination process does not apply may be Green or be assigned a severity level after NRC management review. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is  
The crosscutting aspect is determined using Inspection Manual Chapter 0310, Components
described in NUREG
Within the Cross Cutting Areas. Findings for which the significance determination process
-1649, "Reactor Oversight Process," Revision 4, dated December 2006.
does not apply may be Green or be assigned a severity level after NRC management review.
  A. NRC-Identified Findings and Self
The NRC's program for overseeing the safe operation of commercial nuclear power reactors is
-Revealing Findings
described in NUREG-1649, Reactor Oversight Process, Revision 4, dated December 2006.
    Cornerstone: Initiating Events
A.     NRC-Identified Findings and Self-Revealing Findings
  Green. The inspectors identified a non
        Cornerstone: Initiating Events
-cited violation of 10 CFR Part 50
            *  Green. The inspectors identified a non-cited violation of 10 CFR Part 50,
, Appendix B, Criterion V, "Instructions, Procedures, and Drawings," for a work  
              Appendix B, Criterion V, Instructions, Procedures, and Drawings, for a work
order that did not accomplish a leak seal repair in accordance with its engineering evaluation. Valve BMV0037 is a safety related ASME Code Class
              order that did not accomplish a leak seal repair in accordance with its
2 steam generator blowdown valve that had a body
              engineering evaluation. Valve BMV0037 is a safety related ASME Code Class 2
-to-bonnet steam leak. Wolf Creek and its vendor produced modification documents to perform a leak
              steam generator blowdown valve that had a body-to-bonnet steam leak. Wolf
-seal repair. The inspectors identified
              Creek and its vendor produced modification documents to perform a leak-seal
that on December 10, 2011, Wolf Creek installed an injection port in the valve body in close proximity of another injection port
              repair. The inspectors identified that on December 10, 2011, Wolf Creek installed
Work orders allowed the location of the injection ports to be determined by the work. The pair w as not installed in accordance with change package 9385. After inspector questioning, Wolf Creek performed
              an injection port in the valve body in close proximity of another injection port.
an evaluation that demonstrated that the valve body retained structural integrity
              Work orders allowed the location of the injection ports to be determined by the
. This issue was entered into the corrective action program under condition report  
              work. The pair was not installed in accordance with change package 9385. After
52992. The failure to ensure that the configuration of a safety
              inspector questioning, Wolf Creek performed an evaluation that demonstrated
-related steam generator blowdown was controlled
              that the valve body retained structural integrity. This issue was entered into the
in accordance with the approved engineering change package during leak seal activities is a performance deficiency. This finding was more than minor because it impacted the procedure quality attribute of the Initiating Events Cornerstone and affected the objective to limit the likelihood of those events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Using Inspection Manual Chapter  
              corrective action program under condition report 52992.
0609 , Appendix A, this finding was determined to be of very low safety significance because an evaluation after the modification was able to  
              The failure to ensure that the configuration of a safety-related steam generator
demonstrate structural integrity. Therefore, the finding does not contribute to both the likelihood of a reactor trip and the likelihood that mitigation equipment will not be available. The inspectors identified the cause of the finding had a human performance crosscutting aspect in the area of resources. Specifically, the licensee did not ensure that the work order instructions were complete, accurate, and reflected up
              blowdown was controlled in accordance with the approved engineering change
-to-date design documentation sufficiently to control plant configuration in accordance with design [H.2.c]
              package during leak seal activities is a performance deficiency. This finding was
(Section 1R18)
              more than minor because it impacted the procedure quality attribute of the
.
              Initiating Events Cornerstone and affected the objective to limit the likelihood of
  - 3 - Enclosure   Cornerstone: Mitigating Systems
              those events that upset plant stability and challenge critical safety functions
  Green. A self-revealing non
              during shutdown as well as power operations. Using Inspection Manual Chapter
-cited violation of 10 CFR 50
              0609, Appendix A, this finding was determined to be of very low safety
, Appendix B
              significance because an evaluation after the modification was able to
, Criterion V , "Inspections, Procedures, and Drawings
              demonstrate structural integrity. Therefore, the finding does not contribute to both
," was identified as a result of  
              the likelihood of a reactor trip and the likelihood that mitigation equipment will not
a leaking watertight door that was observed on January 13, 2012. Station  
              be available. The inspectors identified the cause of the finding had a human
procedure MPM X X-002 , "Watertight Door Preventive Maintenance Activities
              performance crosscutting aspect in the area of resources. Specifically, the
," failed to ensure the
              licensee did not ensure that the work order instructions were complete, accurate,
proper position of the alignment screws, which resulted in
              and reflected up-to-date design documentation sufficiently to control plant
leakage through a misalignment between the door and its threshold.
              configuration in accordance with design [H.2.c] (Section 1R18).
  During the January 13, 2012 , loss of offsite power, the  
                                                -2-                               Enclosure
auxiliary building general area sump
 
pumps did not operate for approximately 36
  Cornerstone: Mitigating Systems
hours. Condensed steam and other effluents slowly accrued in the stairwell area outside the  
      *  Green. A self-revealing non-cited violation of 10 CFR 50, Appendix B,
containment  
          Criterion V, Inspections, Procedures, and Drawings, was identified as a result of
spray pump rooms to a depth of 24
          a leaking watertight door that was observed on January 13, 2012. Station
to 36 inches. The train B containment spray pump room watertight
          procedure MPM XX-002, Watertight Door Preventive Maintenance Activities,
door leaked
          failed to ensure the proper position of the alignment screws, which resulted in
approximately 10
          leakage through a misalignment between the door and its threshold. During the
gallons per minute
          January 13, 2012, loss of offsite power, the auxiliary building general area sump
and pooled in both the containment  
          pumps did not operate for approximately 36 hours. Condensed steam and other
spray pump room and the  
          effluents slowly accrued in the stairwell area outside the containment spray pump
residual heat removal pump room to a depth of three inches.
          rooms to a depth of 24 to 36 inches. The train B containment spray pump room
  This issue was entered into the corrective action program under condition report 51622. The licensee corrected the procedure and realigned the affected watertight doors.
          watertight door leaked approximately 10 gallons per minute and pooled in both
  Failure to properly adjust safety
          the containment spray pump room and the residual heat removal pump room to a
-related watertight door alignment screws during testing activities is a performance deficiency. The performance deficiency is more than minor and therefore a finding because, if left uncorrected it could lead to a more significant safety concern. Using Inspection Manual Chapter 0609
          depth of three inches. This issue was entered into the corrective action program
, Appendix A, the finding was characterized using Exhibit 4, "Seismic, Flooding, and Severe Weather Screening Criteria
          under condition report 51622. The licensee corrected the procedure and
.The finding was
          realigned the affected watertight doors.
determined to be of very low safety significance (Green) because the degraded flood protection equipment would not have caused a plant trip or other initiating event, would not degrade two or more trains of a multi
          Failure to properly adjust safety-related watertight door alignment screws during
-train safety system, would not degrade one or more trains of a supporting system, and the finding does not involve the total loss of any safety function.
          testing activities is a performance deficiency. The performance deficiency is
  The inspectors determined the cause of this finding was not indicative of current performance.
          more than minor and therefore a finding because, if left uncorrected it could lead
(Section 1R06)
          to a more significant safety concern. Using Inspection Manual Chapter 0609,
. B. Licensee-Identified Violations
          Appendix A, the finding was characterized using Exhibit 4, Seismic, Flooding,
  A violation of very low safety significance was identified by the licensee and has been reviewed by the inspectors.  
          and Severe Weather Screening Criteria. The finding was determined to be of
Corrective actions taken or planned by the licensee have
          very low safety significance (Green) because the degraded flood protection
been entered into the licensee's corrective action program.
          equipment would not have caused a plant trip or other initiating event, would not
  This violation
          degrade two or more trains of a multi-train safety system, would not degrade one
and associated corrective action tracking numbers are listed in Section 4OA7 of this report.
          or more trains of a supporting system, and the finding does not involve the total
 
          loss of any safety function. The inspectors determined the cause of this finding
 
          was not indicative of current performance. (Section 1R06).
  - 4 - Enclosure REPORT DETAILS
B. Licensee-Identified Violations
  Summary of Plant Status  
  A violation of very low safety significance was identified by the licensee and has been
  Wolf Creek began the inspection period on March 31 at 100
  reviewed by the inspectors. Corrective actions taken or planned by the licensee have
percent power and remained at full power until May 24, when power was reduced to 69
  been entered into the licensees corrective action program. This violation and
percent for planned turbine thermal performance testing. Wolf Creek returned to 100
  associated corrective action tracking numbers are listed in Section 4OA7 of this report.
percent power later on May 24. On June 6, Wolf Creek reduced power to 88
                                            -3-                               Enclosure
percent when it entered Limiting Condition of Operation 3.0.3 due to having the tra in A vital switchgear and battery air conditioning
 
unit inoperable. Wolf Creek returned to 100
                                          REPORT DETAILS
percent power later on June 6
Summary of Plant Status
and remained at 100
Wolf Creek began the inspection period on March 31 at 100 percent power and remained at full
percent for the rest of the inspection period.
power until May 24, when power was reduced to 69 percent for planned turbine thermal
  1. REACTOR SAFETY
performance testing. Wolf Creek returned to 100 percent power later on May 24. On June 6,
  Cornerstones: Initiating Events, Mitigat
Wolf Creek reduced power to 88 percent when it entered Limiting Condition of Operation 3.0.3
ing Systems, and Barrier Integrity
due to having the train A vital switchgear and battery air conditioning unit inoperable. Wolf
  1R01 Adverse Weather Protection (71111.01)
Creek returned to 100 percent power later on June 6 and remained at 100 percent for the rest of
.1 Readiness for Impending Adverse Weather Conditions
the inspection period.
a. Inspection Scope
1.     REACTOR SAFETY
Since thunderstorms with potential tornados and high winds were forecast in the vicinity of the facility for
        Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity
April 14, 2012, the inspectors reviewed the plant personnel's overall preparations/protection for the expected weather conditions. On April 13, 2012, the inspectors walked down the condensate storage tank, demineralized water
1R01 Adverse Weather Protection (71111.01)
storage tank, reactor makeup water, and refueling water storage tank because their functions could be affected , or required
.1     Readiness for Impending Adverse Weather Conditions
, as a result of high winds or tornado
  a.   Inspection Scope
-generated missiles or the loss of offsite power. The inspectors evaluated the plant staff's preparations against the site's procedures and determined that the staff's actions were adequate. During the  
        Since thunderstorms with potential tornados and high winds were forecast in the vicinity
inspection, the inspectors focused on plant
        of the facility for April 14, 2012, the inspectors reviewed the plant personnels overall
-specific design features and the licensee's procedures used to respond to specified adverse weather conditions. The inspectors  
        preparations/protection for the expected weather conditions. On April 13, 2012, the
also toured the plant grounds to look for any loose debris that could become missiles during a tornado. The inspector's
        inspectors walked down the condensate storage tank, demineralized water storage tank,
evaluated operator staffing and accessibility of controls and indications for those systems required to control the plant. Additionally, the inspectors reviewed the Updated Safety Analysis Report (USAR) and performance requirements for the systems selected for inspection, and verified that operator actions were appropriate as specified by plant
        reactor makeup water, and refueling water storage tank because their functions could be
-specific procedures. The inspectors also reviewed a sample of corrective action program items to verify that the licensee
        affected, or required, as a result of high winds or tornado-generated missiles or the loss
-identified adverse weather issues at an appropriate threshold and dispositioned them through the corrective action program in accordance with station corrective action procedures.  
        of offsite power. The inspectors evaluated the plant staffs preparations against the sites
Specific documents reviewed during this inspection are listed in the attachment.
        procedures and determined that the staffs actions were adequate. During the
  Because the storm of April 14, 2012
        inspection, the inspectors focused on plant-specific design features and the licensees
, caused the  
        procedures used to respond to specified adverse weather conditions. The inspectors
temporary diesel-driven fire water pump to be locally shut
        also toured the plant grounds to look for any loose debris that could become missiles
down due to wave action on Coffey County lake, and a second storm with similar behavior was predicted to arrive on April 19, the inspectors reviewed corrective action documents and the temporary fire pump operating procedures.
        during a tornado. The inspectors evaluated operator staffing and accessibility of
  The inspectors
        controls and indications for those systems required to control the plant. Additionally, the
discussed applicable
        inspectors reviewed the Updated Safety Analysis Report (USAR) and performance
equipment and staffing requirements with the  
        requirements for the systems selected for inspection, and verified that operator actions
operations
        were appropriate as specified by plant-specific procedures. The inspectors also
  - 5 - Enclosure superintendent. The inspectors reviewed plans
        reviewed a sample of corrective action program items to verify that the licensee-
to secure the pump during periods of high wave action for the long
        identified adverse weather issues at an appropriate threshold and dispositioned them
-term safety and
        through the corrective action program in accordance with station corrective action
reliability of the pump, and to have the dedicated operator stationed in  
        procedures. Specific documents reviewed during this inspection are listed in the
an adjacent building to restart the pump in the event of an actual fire. The inspectors reviewed station procedures for operation of the  
        attachment.
temporary diesel-driven fire water pump and walked down the pump, as well as the suction, and discharge system connection. The inspectors also walked down the  
        Because the storm of April 14, 2012, caused the temporary diesel-driven fire water pump
electric motor-driven fire water pump and service water pumps in the adjacent  
        to be locally shut down due to wave action on Coffey County lake, and a second storm
circulati ng water screen house building to verify that the area was free from any wind
        with similar behavior was predicted to arrive on April 19, the inspectors reviewed
-driven missiles and that the equipment would be available to respond to a valid demand in the event of a  
        corrective action documents and the temporary fire pump operating procedures. The
fire. Specific documents reviewed are listed in the attachment.
        inspectors discussed applicable equipment and staffing requirements with the operations
  These activities constitute completion of
                                                  -4-                             Enclosure
two readiness for impending adverse weather condition sample
 
s as defined in Inspection Procedu
      superintendent. The inspectors reviewed plans to secure the pump during periods of
re 71111.01-05. b. Findings No findings were identified.
      high wave action for the long-term safety and reliability of the pump, and to have the
  .2 Summer Readiness for Offsite and Alternate
      dedicated operator stationed in an adjacent building to restart the pump in the event of
-ac Power a. Inspection Scope
      an actual fire. The inspectors reviewed station procedures for operation of the
The inspectors performed a review of preparations for summer weather for selected systems, including conditions that could lead to loss-of-offsite power and conditions that could result from high temperatures. The inspectors reviewed the procedures affecting these areas and the communications protocols between the transmission system operator and the plant to verify that the appropriate information was being exchanged when issues arose that could affect the offsite power system. Examples of aspects considered in the inspectors' review included:
      temporary diesel-driven fire water pump and walked down the pump, as well as the
  The coordination between the transmission system operator and the plant's
      suction, and discharge system connection. The inspectors also walked down the electric
operations personnel during off
      motor-driven fire water pump and service water pumps in the adjacent circulating water
-normal or emergency events
      screen house building to verify that the area was free from any wind-driven missiles and
  The explanations for the events
      that the equipment would be available to respond to a valid demand in the event of a
  The estimates of when the offsite power system would be returned to a normal state   The notifications from the transmission system operator to the plant when the offsite power
      fire. Specific documents reviewed are listed in the attachment.
system was returned to normal
      These activities constitute completion of two readiness for impending adverse weather
  During the inspection, the inspectors focused on plant
      condition samples as defined in Inspection Procedure 71111.01-05.
-specific design features and the procedures used by plant personnel to mitigate or respond to adverse weather conditions. Additionally, the inspectors reviewed the USAR and performance requirements for systems selected for inspection, and verified that operator actions were appropriate as specified by plant
  b. Findings
-specific procedures. Specific documents reviewed during this inspection are listed in the attachment. The inspectors also reviewed corrective action program items to verify that the licensee was identifying adverse
      No findings were identified.
  - 6 - Enclosure weather issues at an appropriate threshold and entering them into their corrective action program in accordance with station corrective action procedures.
.2   Summer Readiness for Offsite and Alternate-ac Power
   
  a. Inspection Scope
These activities constitute completion of one readiness for summer weather affect on offsite and alternate
      The inspectors performed a review of preparations for summer weather for selected
-ac power sample as defined in Inspection Procedure
      systems, including conditions that could lead to loss-of-offsite power and conditions that
71111.01-05.  b. Findings No findings were identified.
      could result from high temperatures. The inspectors reviewed the procedures affecting
 
      these areas and the communications protocols between the transmission system
      operator and the plant to verify that the appropriate information was being exchanged
      when issues arose that could affect the offsite power system. Examples of aspects
      considered in the inspectors review included:
          *  The coordination between the transmission system operator and the plants
              operations personnel during off-normal or emergency events
          *  The explanations for the events
          *  The estimates of when the offsite power system would be returned to a normal
              state
          *  The notifications from the transmission system operator to the plant when the
              offsite power system was returned to normal
      During the inspection, the inspectors focused on plant-specific design features and the
      procedures used by plant personnel to mitigate or respond to adverse weather
      conditions. Additionally, the inspectors reviewed the USAR and performance
      requirements for systems selected for inspection, and verified that operator actions were
      appropriate as specified by plant-specific procedures. Specific documents reviewed
      during this inspection are listed in the attachment. The inspectors also reviewed
      corrective action program items to verify that the licensee was identifying adverse
                                                -5-                             Enclosure
 
    weather issues at an appropriate threshold and entering them into their corrective action
    program in accordance with station corrective action procedures.
    These activities constitute completion of one readiness for summer weather affect on
    offsite and alternate-ac power sample as defined in Inspection Procedure 71111.01-05.
  b. Findings
    No findings were identified.
1R04 Equipment Alignment (71111.04)
1R04 Equipment Alignment (71111.04)
  Partial Walkdown
    Partial Walkdown
a. Inspection Scope
The inspectors performed partial system walkdowns of the following risk
-significant systems:  April 14, 2012, Auxiliary
building watertight
doors and internal flood barriers with train B emergency core cooling watertigh t door out of service  June 19, 2012, Boron injection tank depressurization
flowpath through the
safety injection test line 
The inspectors selected these systems based on their risk significance relative to the
Reactor Safety Cornerstones at the time they were inspected.  The inspectors attempted to identify any discrepancies that could affect the function of the system, and, therefore,
potentially increase risk.  The inspectors reviewed applicable operating procedures, system diagrams, USAR, technical specification requirements, administrative technical specifications, outstanding work orders, condition reports, and the impact of ongoing work activities on redundant trains of equipment in order to identify conditions that could have rendered the systems incapable of performing their intended functions.  The inspectors also inspected accessible portions of the systems to verify system components and support equipment were aligned correctly and operable.  The
inspectors examined the material condition of the components and observed operating parameters of equipment to verify that there were no obvious deficiencies.  The inspectors also verified that the licensee had properly identified and resolved equipment alignment problems that could cause initiating events or impact the capability of mitigating systems or barriers and entered them into the corrective action program with the appropriate significance characterization.  Specific documents reviewed during this inspection are listed in the attachment.
  These activities constitute completion of
two partial system walkdown sample
s as defined in Inspection Procedure
71111.04-05.  b. Findings No findings were identified.
 
  - 7 - Enclosure  1R05 Fire Protection (71111.05)
  Quarterly Fire Inspection Tours
a. Inspection Scope
The inspectors conducted fire protection walkdowns that were focused on availability, accessibility, and the condition of firefighting equipment in the following risk
-significant plant areas:
  April 4, 2012
, Train A motor-driven auxiliary feedwater pump and valve rooms  April 4, 2012
, Train B motor-driven auxiliary feedwater pump and valve rooms  April 5, 2012 , Turbine-driven auxiliary feedwater pump and valve rooms  The inspectors reviewed areas to assess if licensee personnel had implemented a fire protection program that adequately controlled combustibles and ignition sources within the plant; effectively maintained fire detection and suppression capability; maintained passive fire protection features in good material condition; and had implemented adequate compensatory measures for out of service, degraded or inoperable fire protection equipment, systems, or features, in accordance with the licensee's fire plan.  The inspectors selected fire areas based on their overall contribution to internal fire risk as documented in the plant's Individual Plant Examination of External Events with later additional insights, their potential to affect equipment that could initiate or mitigate a plant transient, or their impact on the plant's ability to respond to a security event.  Using the documents listed in the attachment, the inspectors verified that fire hoses and extinguishers were in their designated locations and available for immediate use; that fire detectors and sprinklers were unobstructed; that transient material loading was within the analyzed limits; and fire doors, dampers, and penetration seals appeared to
be in satisfactory condition.  The inspectors also verified that minor issues identified during the inspection were entered into the licensee's corrective action program.  Specific documents reviewed during this inspection are listed in the attachment.
 
These activities constitute completion of three quarterly fire-protection inspection sample s as defined in Inspection Procedure
71111.05-05.  b. Findings No findings were identified.
  1R06 Flood Protection Measures (71111.06)
a. Inspection Scope
The inspectors reviewed the USAR , the flooding analysis, and plant procedures to assess susceptibilities involving internal flooding; reviewed the corrective action program to determine if licensee personnel identified and corrected flooding problems; inspected underground bunkers/manholes to verify the adequacy of sump pumps, level alarm circuits, cable splices subject to submergence, and drainage for bunkers/manholes; and 
  - 8 - Enclosure verified that operator actions for coping with flooding can reasonably achieve the desired outcomes.  The inspectors also inspected the areas listed below to verify the adequacy of equipment seals located below the flood line, floor and wall penetration seals, watertight door seals, common drain lines and sumps, sump pumps, level alarms, and control circuits, and temporary or removable flood barriers.  Specific documents
reviewed during this inspection are listed in the attachment.    April 17, 2012 , Containment
spray train B and
residual heat removal train B pump rooms  These activities constitute completion of one flood protection measures inspection sample as defined in Inspection Procedure
71111.06-05.  b. Findings Introduction.
  A Green, self
-revealing, non
-cited violation of 10 CFR 50
, Appendix B
, Criterion V
, "Inspections, Procedures, and Drawings
," was identified as a result of
a leaking watertight door that was observed on January 13, 2012.  Station Procedure
MP M XX-002 "Watertight Door Preventive Maintenance Activities
," failed to ensure the
proper position of the alignment screws, which resulted in
leakage through a misalignment between the door and its threshold.
Description.
  On January 13, 2012, Wolf Creek tripped due to a main generator breaker fault.  Many non-safety systems were without power
for several days until temporary power could be arranged.  One such system was the
auxiliary building general area sumps, which were without power for approximately 36 hours.  Condensed steam and
other effluents slowly accrued
in the stairwell area outside the
containment
spray pump rooms.  The containment spray pump rooms lead to the corresponding
train residual heat removal pump rooms.  Each train of containment spray pump rooms
is separated from the stairwell
by a watertight door.  There is no flood protection between the corresponding
containment
spray and residual heat removal pump rooms.  Over
the 36-hour period without power
, the general area water level rose to approximately 24 to
30 inches in depth, which was above the bottom of the watertight doors.  The train A containment
spray pump room door passed minimal leakage with no impact to safet y-related equipment in the rooms.  The
train B containment
spray pump room door passed an unacceptable amount
of leakage estimated to be approximately 10
gpm and pooled into
both the containment
spray pump room and the
residual heat removal pump room to a depth of three inches.
On April 17, 2012, Wolf Creek identified that
a previous condition report screening resulted in a nonconservative operability assessment of door leakage.
  The licensee discovered that corrective actions had not been taken
and at 2:53 p.m., control room operators promptly declared the door and the train
B containment
spray and train
B residual heat removal pumps inoperable and entered the appropriate
technical specification
action statements.  The licensee inspected the material condition of the gasket and determined that it met the requirements of its preventive maintenance activity detailed in station procedure MPM
XX-002 , "Watertight Doors Preventive Maintenance Activity."  At that point
, the licensee determined that the procedure must be in some way inadequate.  The licensee contacted another facility
for information and compared their 
  - 9 - Enclosure respective procedures.  The licensee
determined that another facility
was regularly adjusting the doors
' alignment screws ("dog ears") whereas Wolf Creek's procedure directed the mechanic to skip that step if the door passed its chalk test in the previous step.    The chalk test checks engagement between the door frame and the door seal.  Operations personnel determined that the chalk test ha
d a high likelihood of producing a false positive because the chalk is transferred around the entire perimeter of the seal when the mechanic closes the door, appearing to demonstrate a proper seal.
  However, actual sealing occurs when the hand wheel is turned to engage the dog ears.  If the dog ears are properly aligned, the door will seal around the entire seating surface.  However
, if they are loose, the door may rest ajar in the threshold allowing water to pass.  A field inspection observed that six of eight dog ears were loose on the
containment
spray room B watertight door, whereas only two of eight dog ears on the train
A door were loose and it performed satisfactorily under the same flood conditions.  The licensee completed the adjustments of the to the alignment screws, door jamb welding, and seal replacement
  and returned the train
B containment spray and emergency core cooling systems to service at 2:48
p.m. on April 18, 2011.
Analysis.  Failure to properly adjust safety
-related watertight door alignment screws during testing activities is a performance deficiency.  The performance deficiency is more than minor
, and therefore a finding because, if left uncorrected it could lead to a more significant safety concern.  Using Inspection Manual Chapter 0609
, Appendix A, the finding was characterized under the Exhibit 4, "Seismic, Flooding, and Severe Weather Screening Criteria
."  The finding was
determined to be of very low safety significance (Green) because the degraded flood protection equipment would not have caused a plant trip or other initiating event, would not degrade two or more trains of a multi-train safety system, would not degrade one or more trains of a supporting system, and the finding does not involve the total loss of any safety function.
The inspectors determined the cause of this finding was not indicative of current performance.
Enforcement.  Title 10 CFR 5 0 , Appendix B
, Criterion V
, states that
: "Activities affecting quality shall be prescribed by documented instructions, procedures, or drawings of a type appropriate to the circumstances and shall be accomplished in accordance with these instructions, procedures, or drawings.
"  Instructions, procedures, or drawings shall include appropriate quantitative or qualitative acceptance criteria for determining that
important activities have been satisfactorily accomplished.  Procedure MPM XX-002 , "Watertight
Doors Preventive Maintenance Activity,"
Revision 4 , a safety-related procedure, was intended to implement activities affecting quality
for flood doors.
  Contrary to the above, from original plant construction in 1985 through April
18, 2012, the licensee performed activities affecting the quality of watertight doors using a procedure that was not appropriate to the circumstances.  Specifically, Wolf Creek station procedure MPM
XX-002 , "Watertight Doors Preventive Maintenance Activity,"
Revisio n 4 , failed to ensure the
proper position of the door alignment screws, which resulted in
leakage due to misalignment.
  Because this finding is of very low safety significance and was entered into the licensee corrective action program as
condition
report 51622, this violation is being treated as a non
-cited violation in accordance with Section 2.3.2 of the Enforcement Policy: NCV 05000482/2012003
-01 , "Unacceptable Leakage Through Safety
-Related Watertight Door
During Loss of Offsite Power.
  - 10 - Enclosure 1R11    Licensed Operator Requalification Program and Licensed Operator Performance (71111.11)
  .1        Quarterly Review of Licensed Operator Requalification Program  a.    Inspection Scope
  On June 18, 2012, the inspectors observed a crew of licensed operators in the plant's simulator during requalification testing.
  The inspectors assessed the following areas:
  Licensed operator performance
  The ability of the licensee to administer the evaluations
  The modeling and performance of the control room simulator
  The quality of post
-scenario critiques
  Followup actions taken by the licensee for identified discrepancies
  These activities constitute completion of one quarterly licensed operator requalification program sample as defined in Inspection Procedure
71111.11.  b.    Findings  No findings were identified.
  .2        Quarterly Observation of Licensed Operator Performance
   a. Inspection Scope
   a. Inspection Scope
   On the evening of April 5, 2012, the inspectors
    The inspectors performed partial system walkdowns of the following risk-significant
observed the performance of on
    systems:
-shift licensed operators in
          *   April 14, 2012, Auxiliary building watertight doors and internal flood barriers with
the plant's main control room.
              train B emergency core cooling watertight door out of service
At the time of the observations, the plant was in a period of heightened activity
          *  June 19, 2012, Boron injection tank depressurization flowpath through the safety
due to Security Force on Force drills being conducted throughout the plant
              injection test line
. The inspectors observed the operators' performance of the following activities:
    The inspectors selected these systems based on their risk significance relative to the
  Shift turnover
    Reactor Safety Cornerstones at the time they were inspected. The inspectors attempted
brief  Drill communication brief
    to identify any discrepancies that could affect the function of the system, and, therefore,
  Routine reactivity
    potentially increase risk. The inspectors reviewed applicable operating procedures,
manipulations
    system diagrams, USAR, technical specification requirements, administrative technical
.  In addition, the inspectors assessed the operators' adherence to plant procedures, including procedure AP 21-001 , "Conduct of Operations
    specifications, outstanding work orders, condition reports, and the impact of ongoing
," and other operations department policies.
    work activities on redundant trains of equipment in order to identify conditions that could
  These activities constitute completion of one quarterly licensed
    have rendered the systems incapable of performing their intended functions. The
-operator performance sample as defined in Inspection Procedure
    inspectors also inspected accessible portions of the systems to verify system
71111.11.  b.  Findings  No findings were identified.
    components and support equipment were aligned correctly and operable. The
 
    inspectors examined the material condition of the components and observed operating
  - 11 - Enclosure 1R12 Maintenance Effectiveness (71111.12) a. Inspection Scope
    parameters of equipment to verify that there were no obvious deficiencies. The
The inspectors evaluated degraded performance issues involving the following risk significant systems:
    inspectors also verified that the licensee had properly identified and resolved equipment
  May 15, 2012, Startup
    alignment problems that could cause initiating events or impact the capability of
main feedwater pump performance monitoring , maintenance rule function AE
    mitigating systems or barriers and entered them into the corrective action program with
-04  June 21, 2012, Reactor
    the appropriate significance characterization. Specific documents reviewed during this
protection
    inspection are listed in the attachment.
system card replacements , maintenance
    These activities constitute completion of two partial system walkdown samples as
rule function SP
    defined in Inspection Procedure 71111.04-05.
-02  The inspectors reviewed events such as where ineffective equipment maintenance has resulted in valid or invalid automatic actuations of engineered safeguards systems and independently verified the licensee's actions to address system performance or condition problems in terms of the following:
  b. Findings
  Implementing appropriate work practices
    No findings were identified.
  Identifying and addressing common cause failures
                                              -6-                                Enclosure
  Scoping of systems in accordance with 10 CFR 50.65(b)
 
  Characterizing system reliability issues for performance
1R05 Fire Protection (71111.05)
monitoring
    Quarterly Fire Inspection Tours
  Charging unavailability for performance
  a. Inspection Scope
monitoring
    The inspectors conducted fire protection walkdowns that were focused on availability,
  Trending key parameters for condition monitoring
    accessibility, and the condition of firefighting equipment in the following risk-significant
  Ensuring proper classification in accordance with 10
    plant areas:
CFR 50.65(a)(1) or
          *  April 4, 2012, Train A motor-driven auxiliary feedwater pump and valve rooms
-(a)(2)  Verifying appropriate performance criteria for structures, systems, and components classified as having an adequate demonstration of performance through preventive maintenance, as described in 10 CFR 50.65(a)(2), or as requiring the establishment of appropriate and adequate goals and corrective actions for systems classified as not having adequate performance, as described in 10 CFR 50.65(a)(1)
          *  April 4, 2012, Train B motor-driven auxiliary feedwater pump and valve rooms
 
          *  April 5, 2012, Turbine-driven auxiliary feedwater pump and valve rooms
The inspectors assessed performance issues with respect to the reliability, availability, and condition monitoring of the system. In addition, the inspectors verified maintenance effectiveness issues were entered into the corrective action program with the appropriate significance characterization. Specific documents reviewed during this inspection are  
    The inspectors reviewed areas to assess if licensee personnel had implemented a fire
listed in the attachment.
    protection program that adequately controlled combustibles and ignition sources within
 
    the plant; effectively maintained fire detection and suppression capability; maintained
These activities constitute completion of
    passive fire protection features in good material condition; and had implemented
two quarterly maintenance effectiveness sample s as defined in Inspection Procedure
    adequate compensatory measures for out of service, degraded or inoperable fire
71111.12-05.  
    protection equipment, systems, or features, in accordance with the licensees fire plan.
   - 12 - Enclosure b. Findings No findings were identified.
    The inspectors selected fire areas based on their overall contribution to internal fire risk
  1R13 Maintenance Risk Assessments and Emergent Work
    as documented in the plants Individual Plant Examination of External Events with later
Control (71111.13)
    additional insights, their potential to affect equipment that could initiate or mitigate a
a. Inspection Scope
    plant transient, or their impact on the plants ability to respond to a security event. Using
The inspectors reviewed licensee personnel's evaluation and management of plant risk for the maintenance and emergent work activities affecting risk
    the documents listed in the attachment, the inspectors verified that fire hoses and
-significant and safety
    extinguishers were in their designated locations and available for immediate use; that
-related equipment listed below to verify that the appropriate risk assessments were performed prior to removing equipment for work:
    fire detectors and sprinklers were unobstructed; that transient material loading was
  April 10 and 15, 2012, NK02 DC bus voltage and current fluctuations
    within the analyzed limits; and fire doors, dampers, and penetration seals appeared to
  The inspectors selected these activities based on potential risk significance relative to the R eactor Safety Cornerstones.  As applicable for each activity, the inspectors verified that licensee personnel performed risk assessments as required by 10
    be in satisfactory condition. The inspectors also verified that minor issues identified
CFR 50.65(a)(4) and that the assessments were accurate and complete.  When licensee personnel performed emergent work, the inspectors verified that the licensee personnel promptly assessed and managed plant risk. The inspectors reviewed the scope of maintenance
    during the inspection were entered into the licensees corrective action program.
work, discussed the results of the assessment with the licensee's probabilistic risk analyst or shift technical advisor, and verified plant conditions were consistent with the risk assessment.  The inspectors also reviewed the technical specification requirements and inspected portions of redundant safety systems, when applicable, to verify risk analysis assumptions were valid and applicable requirements were met. Specific documents reviewed during this inspection are listed in the attachment.
    Specific documents reviewed during this inspection are listed in the attachment.
  These activities constitute completion of
    These activities constitute completion of three quarterly fire-protection inspection
one maintenance risk assessments and emergent work control inspection sample as defined in Inspection Procedure 71111.13-05.  b. Findings No findings were identified.
    samples as defined in Inspection Procedure 71111.05-05.
  1R15 Operability Evaluations
   b. Findings
and Functionality Assessments
    No findings were identified.
(71111.15)
1R06 Flood Protection Measures (71111.06)
a. Inspection Scope
  a. Inspection Scope
The inspectors reviewed the following issues:
    The inspectors reviewed the USAR, the flooding analysis, and plant procedures to
   April 13, 2012, Chemical and volume control system alternate charging line
    assess susceptibilities involving internal flooding; reviewed the corrective action program
check valve s BBV8379A and BBV8379B potential stud degradation
    to determine if licensee personnel identified and corrected flooding problems; inspected
   April 18, 2012, Flood door operability in Auxiliary Building
    underground bunkers/manholes to verify the adequacy of sump pumps, level alarm
   May 2, 2012, Operator Manual Actions for control room ventilation damper
    circuits, cable splices subject to submergence, and drainage for bunkers/manholes; and
GKD-181 
                                                -7-                              Enclosure
  - 13 - Enclosure  May 23, 2012, Refueling
 
water storage tank valve BNV-11 manual actions during sump recirculation
  verified that operator actions for coping with flooding can reasonably achieve the desired
   June 16, 2012, Vital Switchgear room temperatures after loss of train B air conditioning unit
  outcomes. The inspectors also inspected the areas listed below to verify the adequacy
   January 24
  of equipment seals located below the flood line, floor and wall penetration seals,
and February 13, 2012, residual heat remov
  watertight door seals, common drain lines and sumps, sump pumps, level alarms, and
al transients following
  control circuits, and temporary or removable flood barriers. Specific documents
non-vital power loss
  reviewed during this inspection are listed in the attachment.
with normal service water running in Mode 5
      *  April 17, 2012, Containment spray train B and residual heat removal train B
  The inspectors selected these potential operability issues based on the risk
          pump rooms
significance of the associated components and systems. The inspectors evaluated the technical adequacy of the evaluations to ensure that technical specification operability was properly justified and the subject component or system remained available such that no unrecognized increase in risk occurred.  The inspectors compared the operability
  These activities constitute completion of one flood protection measures inspection
and design criteria in the appropriate sections of the technical specifications and USAR to the licensee
  sample as defined in Inspection Procedure 71111.06-05.
personnel's
b. Findings
evaluations to determine whether the components or systems were operable.  Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended
  Introduction. A Green, self-revealing, non-cited violation of 10 CFR 50, Appendix B,
and were properly controlled. The inspectors determined, where appropriate, compliance with bounding limitations associated with the evaluations.  Additionally, the inspectors also reviewed a sampling of corrective action documents to verify that the licensee was identifying and correcting any deficiencies associated with operability evaluations. Specific documents reviewed during this inspection are listed in the attachment.  These activities constitute completion of six operability evaluation inspection samples as defined in Inspection Procedure
  Criterion V, Inspections, Procedures, and Drawings, was identified as a result of a
71111.15-0 5.  b. Findings No findings were identified.
  leaking watertight door that was observed on January 13, 2012. Station Procedure
  1R18 Plant Modifications (71111.18)
  MPM XX-002 Watertight Door Preventive Maintenance Activities, failed to ensure the
  Temporary Modifications
   proper position of the alignment screws, which resulted in leakage through a
a. Inspection Scope
  misalignment between the door and its threshold.
To verify that the safety functions of important safety systems were not degraded, the inspectors reviewed the temporary modification
   Description. On January 13, 2012, Wolf Creek tripped due to a main generator breaker
for leak seal repair of steam generator tube sheet drain valve BMV0037
   fault. Many non-safety systems were without power for several days until temporary
The inspectors reviewed the temporary modification and the associated safety
  power could be arranged. One such system was the auxiliary building general area
-evaluation screening against the system design bases documentation, including the USAR and the technical specifications, and verified that the modification did not adversely affect the system operability/availability. The inspectors also verified that the installation and restoration were consistent with the modification documents and that configuration control was adequate. Additionally, the inspectors verified that the 
  sumps, which were without power for approximately 36 hours. Condensed steam and
  - 14 - Enclosure temporary modification was identified on
  other effluents slowly accrued in the stairwell area outside the containment spray pump
control room drawings, appropriate tags were placed on the affected equipment, and licensee personnel evaluated the combined effects on mitigating systems and the integrity of radiological barriers.
   rooms. The containment spray pump rooms lead to the corresponding train residual
 
   heat removal pump rooms. Each train of containment spray pump rooms is separated
These activities constitute completion of
  from the stairwell by a watertight door. There is no flood protection between the
one sample for temporary plant modifications as defined in Inspection Procedure
  corresponding containment spray and residual heat removal pump rooms. Over the
71111.18-05.  b. Findings Introduction.  The inspectors identified a
  36-hour period without power, the general area water level rose to approximately 24 to
Green non-cited violation of 10 CFR Part 50
  30 inches in depth, which was above the bottom of the watertight doors. The train A
, Appendix B, Criterion V, "Instructions, Procedures, and Drawings," for a work order that did not accomplish a leak seal repair in accordance with its engineering evaluation.
  containment spray pump room door passed minimal leakage with no impact to
  Description.  Valve BMV0037 is a
  safety-related equipment in the rooms. The train B containment spray pump room door
2-inch safety
  passed an unacceptable amount of leakage estimated to be approximately 10 gpm and
-related ASME Code Class 2 valve that isolates the steam generator
  pooled into both the containment spray pump room and the residual heat removal pump
B tube sheet drain. This diaphragm type valve is not required to change position but it is required to be a pressure boundary for the
  room to a depth of three inches.
secondary side of the steam generator. This safety
  On April 17, 2012, Wolf Creek identified that a previous condition report screening
-related quality valve is normally closed and cannot be isolated from the steam generator. 
  resulted in a nonconservative operability assessment of door leakage. The licensee
  On September 9, 2010 , Wolf Creek experienced a leak at the body
  discovered that corrective actions had not been taken and at 2:53 p.m., control room
-to-bonnet joint for valve BMV0037.  Wolf Creek engineering utilized a previously approved a leak seal
  operators promptly declared the door and the train B containment spray and train B
repair using configuration change package 9385.  Change package 13482 re
  residual heat removal pumps inoperable and entered the appropriate technical
-approved change package 9385 for use.  This change package approved drilling injection ports
  specification action statements. The licensee inspected the material condition of the
into the valve body.  On September 30, 2010, Wolf Creek and its contractor drilled two injection ports 180 degrees apart on valve BMV0037 and injected leak sealant.  From September 30, 2010
  gasket and determined that it met the requirements of its preventive maintenance activity
, to November 30, 2011, valve BMV0037 leaked and was injected four times.  On December 5, 2011, BMV0037 began leaking again
  detailed in station procedure MPM XX-002, Watertight Doors Preventive Maintenance
and a third injection port was installed.   The inspectors selected the inspection because the valve had leaked multiple times and was not replaced. The inspectors made a containment entry on March 27, 2012
  Activity. At that point, the licensee determined that the procedure must be in some way
, and observed the sealant injection.  The inspectors observed two injection ports drilled at angles to the valve body in close proximity to one another and a third approximately 180
  inadequate. The licensee contacted another facility for information and compared their
degrees on the other side of the valve body. Two of the injection ports were visually estimated at three quarters of an inch apart
                                            -8-                            Enclosure
and at a shallow angle to the valve body.  Valve BMV0037 was injected again on March 28, 2012 , and May 8, 2012.
 
  The inspectors reviewed work order 10
respective procedures. The licensee determined that another facility was regularly
-333183-002 that was used on September 30, 2010 , to install the injection ports.  The inspectors found no instructions in work order 10-333183-002 for the orientation of the drilling for the injection ports, although they were drilled 180 degrees apart.  Step 1.7.5 of work order 10
adjusting the doors alignment screws (dog ears) whereas Wolf Creeks procedure
-333183-002 stated that the activity was not to exceed three injection ports. The inspectors reviewed work order 11-346576-006 , which installed a third injection port on December 10, 2011, adjacent to one of the existing injection ports. The inspectors noted that Step 1.8.4 of work order 11
directed the mechanic to skip that step if the door passed its chalk test in the previous
-346576-006 allowed the location of the third injection port to be determined by the vendor technician
step.
, and also noted that the third injection port
The chalk test checks engagement between the door frame and the door seal.
was not installed in
Operations personnel determined that the chalk test had a high likelihood of producing a
accordance with change package 9385.
false positive because the chalk is transferred around the entire perimeter of the seal
    
when the mechanic closes the door, appearing to demonstrate a proper seal. However,
   - 15 - Enclosure The inspectors concluded that, despite repeated re
actual sealing occurs when the hand wheel is turned to engage the dog ears. If the dog
-injections, Wolf Creek did not exceed the evaluated limits for the amount of sealant allowed to be injected. However, t he inspectors noted that Wolf Creek's leak seal process did not require a valve with a temporary leak seal repair to be replaced at the next outage, and it did not include
ears are properly aligned, the door will seal around the entire seating surface. However,
a
if they are loose, the door may rest ajar in the threshold allowing water to pass. A field
caution that cooling down a hot system was likely to cause changes in the sealant
inspection observed that six of eight dog ears were loose on the containment spray room
properties and result in another leak.  The inspectors questioned why the valve was not replaced during the previous refueling outage or the forced outage
B watertight door, whereas only two of eight dog ears on the train A door were loose and
and were told that
it performed satisfactorily under the same flood conditions. The licensee completed the
Wolf Creek had had difficulty
adjustments of the to the alignment screws, door jamb welding, and seal replacement
locating a replacement
and returned the train B containment spray and emergency core cooling systems to
valve.
service at 2:48 p.m. on April 18, 2011.
The inspectors reviewed configuration change packages 13482 and 9385. The inspectors noted that configuration change package 9385 stated that three injection ports shall be installed 120 degrees apart around the circumference of the valve body.   
Analysis. Failure to properly adjust safety-related watertight door alignment screws
The holes for those injection ports were said not
during testing activities is a performance deficiency. The performance deficiency is
to require reinforcement because ASME Code Section III, NC
more than minor, and therefore a finding because, if left uncorrected it could lead to a
-3332.1 does not requir
more significant safety concern. Using Inspection Manual Chapter 0609, Appendix A,
e reinforcement since the injection ports are less than 2
the finding was characterized under the Exhibit 4, Seismic, Flooding, and Severe
-inch nominal pipe size. ASME Code Section III
Weather Screening Criteria. The finding was determined to be of very low safety
, article NC
significance (Green) because the degraded flood protection equipment would not have
-3300 is for pressure vessels.  The inspectors, with assistance from the Office of Nuclear Reactor Regulation, determined
caused a plant trip or other initiating event, would not degrade two or more trains of a
that the use of article NC
multi-train safety system, would not degrade one or more trains of a supporting system,
-3300 was reasonable, but the application of article NC
and the finding does not involve the total loss of any safety function. The inspectors
-3332.1 was not appropriate for multiple openings in a
determined the cause of this finding was not indicative of current performance.
valve body. The inspectors questioned if the reinforcement requirements of article NC
Enforcement. Title 10 CFR 50, Appendix B, Criterion V, states that: Activities affecting
-3330 were met.  Wolf Creek subsequently evaluated the article NC
quality shall be prescribed by documented instructions, procedures, or drawings of a
-3330 reinforcement criteria using dimensions reasonably estimated from a photo and the manufacturer's valve drawing. The inspectors concluded that the evaluation did not include the angles of the injection ports.  Drilling the injection ports at an angle other than 90 degrees (to the valve body) results in a deeper hole to reach the body
type appropriate to the circumstances and shall be accomplished in accordance with
-to-bonnet threaded joint (the area where the sealant was injected). This require d more surrounding re
these instructions, procedures, or drawings. Instructions, procedures, or drawings shall
-enforcement material.  The inspectors again questioned the loss of material, this time due to the additional material lost to the injection port angles.  Wolf Creek subsequently took actual measurements during a containment entry and re-performed the ASME Code evaluation. The evaluation considered the angled injection ports to be oval shaped holes through
include appropriate quantitative or qualitative acceptance criteria for determining that
the wall of the valve body per article NC
important activities have been satisfactorily accomplished. Procedure MPM XX-002,
-3331(a). This increased the amount of material required for reinforcement.  The inspectors reviewed the calculation and concluded that the reinforcement requirements were met.
Watertight Doors Preventive Maintenance Activity, Revision 4, a safety-related
   Analysis.  The failure to ensure that the configuration of a safety
procedure, was intended to implement activities affecting quality for flood doors.
-related steam generator blowdown valve was controlled in accordance with the approved engineering change package during leak seal activities is a performance deficiency.  This finding was more than minor because it impacted the procedure quality attribute of the Initiating Events Cornerstone
Contrary to the above, from original plant construction in 1985 through April 18, 2012,
, and it affected the objective to limit the likelihood of those events that upset plant stability and challenge critical safety functions during shutdown as well as power operations.  Using Inspection Manual Chapter 0609
the licensee performed activities affecting the quality of watertight doors using a
, Appendix A, "The Significance Determination Process (SDP) for Findings At
procedure that was not appropriate to the circumstances. Specifically, Wolf Creek
-Power," this finding was determined to be of very low safety significance because an evaluation after the modification was able to demonstrate structural integrity.
station procedure MPM XX-002, Watertight Doors Preventive Maintenance Activity,
Therefore, the finding does not contribute to both the likelihood of a reactor trip and the likelihood that mitigation equipment will not be available.  The inspectors identified the cause of the finding had a in the human performance crosscutting aspect in the area of resources. Specifically, the licensee did not ensure that the work order instructio
Revision 4, failed to ensure the proper position of the door alignment screws, which
ns were sufficiently complete, accurate and reflected up
resulted in leakage due to misalignment. Because this finding is of very low safety
-to-date design documentation
significance and was entered into the licensee corrective action program as condition
sufficient
report 51622, this violation is being treated as a non-cited violation in accordance with
to control plant configuration in accordance with design [H.2.c
Section 2.3.2 of the Enforcement Policy: NCV 05000482/2012003-01, Unacceptable
.] 
Leakage Through Safety-Related Watertight Door During Loss of Offsite Power.
   - 16 - Enclosure  Enforcement.  Title 10 CFR Part 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings," requires, in part, that activities affecting quality shall be prescribed by documented instructions, procedures, or drawings, of a type appropriate to the circumstances and shall be accomplished in accordance with these instructions,
                                          -9-                               Enclosure
procedures, or drawings.  Instructions, procedures, or drawings shall include acceptance criteria for determining that activities have been satisfactorily accomplished.  
 
Wolf Creek
1R11    Licensed Operator Requalification Program and Licensed Operator Performance
configuration change package 9385
      (71111.11)
allowed up to three injection ports 120 degrees
.1    Quarterly Review of Licensed Operator Requalification Program
apart on the valve body.
   a.   Inspection Scope
  Contrary to the above, on September 30, 2010, the licensee performed an activity affecting quality using documented instructions that were not
      On June 18, 2012, the inspectors observed a crew of licensed operators in the plants
appropriate to the circumstances.  Work order 10-333183-002 contained no instructions for the modification of the safety
      simulator during requalification testing. The inspectors assessed the following areas:
-related valve BMV0037 by installing injection ports. Specifically, there were no instructions or acceptance criteria for injection port positioning or orientation, even though the position and orientation to the drilled holes
          *    Licensed operator performance
affect the
          *    The ability of the licensee to administer the evaluations
structural integrity
          *    The modeling and performance of the control room simulator
of the valve body. Because this issue was determined to be of very low safety significance (Green) and was entered into the
          *    The quality of post-scenario critiques
licensee's corrective action program as
          *    Followup actions taken by the licensee for identified discrepancies
condition report 52992, this violation is being treated as a non-cited violation in accordance with Section VI.A.1 of the NRC Enforcement Policy: NCV 05000482/2012003
      These activities constitute completion of one quarterly licensed operator requalification
-0 2, "Incorrect
      program sample as defined in Inspection Procedure 71111.11.
Leak Seal Injection Port Installation."
  b. Findings
 
      No findings were identified.
1R19 Post Maintenance Testing (71111.19)
.2    Quarterly Observation of Licensed Operator Performance
a. Inspection Scope
  aInspection Scope
The inspectors reviewed the following postmaintenance activities to verify that procedures and test activities were adequate to ensure system operability and functional capability:
      On the evening of April 5, 2012, the inspectors observed the performance of on-shift
  May 31, 2012, Vital
      licensed operators in the plants main control room. At the time of the observations, the
switchgear
      plant was in a period of heightened activity due to Security Force on Force drills being
cooler SGK05B after compressor replacement
      conducted throughout the plant. The inspectors observed the operators performance of
  June 21, 2012, Containment
      the following activities:
spray room cooler after inspection
          *    Shift turnover brief
  June 18-25, 2012, Over
          *    Drill communication brief
-temperature delta
          *    Routine reactivity manipulations.
-temperature circuit card replacements
      In addition, the inspectors assessed the operators adherence to plant procedures,
  The inspectors selected these activities based upon the structure, system, or component's ability to affect risk.
      including procedure AP 21-001, Conduct of Operations, and other operations
The inspectors evaluated these activities for the following (as applicable):
      department policies.
  The effect of testing on the plant had been adequately addressed; testing was adequate for the maintenance performed
      These activities constitute completion of one quarterly licensed-operator performance
  Acceptance criteria were clear and demonstrated operational
      sample as defined in Inspection Procedure 71111.11.
readiness; test instrumentation was appropriate
  b. Findings
  The inspectors evaluated the activities against the technical specifications, the USAR , 10 CFR Part 50 requirements, licensee procedures, and various NRC generic communications to ensure that the test results adequately ensured that the equipment met the licensing basis and design requirements.  In addition, the inspectors reviewed corrective action documents associated with postmaintenance tests to determine whether the licensee was identifying problems and
      No findings were identified.
entering them in the corrective action program and that the problems were being corrected commensurate with their 
                                                - 10 -                          Enclosure
  - 17 - Enclosure importance to safety.  Specific documents reviewed during this inspection are listed in the attachment.
 
 
1R12 Maintenance Effectiveness (71111.12)
These activities constitute completion of three postmaintenance testing inspection sample s as defined in Inspection Procedure
  a. Inspection Scope
71111.19-05.  b. Findings No findings were identified.
    The inspectors evaluated degraded performance issues involving the following risk
  1R22 Surveillance Testing (71111.22)
    significant systems:
a. Inspection Scope
          *   May 15, 2012, Startup main feedwater pump performance monitoring,
 
              maintenance rule function AE-04
The inspectors reviewed the USAR, procedure requirements, and technical specifications to ensure that the surveillance activities listed below demonstrated that the systems, structures, and/or components tested were capable of performing their intended safety functions.  The inspectors either witnessed or reviewed test data to verify that the significant surveillance test attributes were adequate to address the following:
          *  June 21, 2012, Reactor protection system card replacements, maintenance rule
  Preconditioning
              function SP-02
  Evaluation of testing impact on the plant
    The inspectors reviewed events such as where ineffective equipment maintenance has
  Acceptance criteria
    resulted in valid or invalid automatic actuations of engineered safeguards systems and
  Test equipment
    independently verified the licensee's actions to address system performance or condition
  Procedures
    problems in terms of the following:
  Jumper/lifted lead controls
          *  Implementing appropriate work practices
  Test data  Testing frequency and method demonstrated technical specification operability
          *  Identifying and addressing common cause failures
  Test equipment removal
          *  Scoping of systems in accordance with 10 CFR 50.65(b)
  Restoration of plant systems
          *  Characterizing system reliability issues for performance monitoring
  Fulfillment of ASME Code requirements
          *  Charging unavailability for performance monitoring
  Updating of performance indicator data
          *  Trending key parameters for condition monitoring
  Engineering evaluations, root causes, and bases for returning tested systems,
          *  Ensuring proper classification in accordance with 10 CFR 50.65(a)(1) or -(a)(2)
structures, and components not meeting the test acceptance criteria were correct
          *   Verifying appropriate performance criteria for structures, systems, and
 
              components classified as having an adequate demonstration of performance
  - 18 - Enclosure  Reference setting data
              through preventive maintenance, as described in 10 CFR 50.65(a)(2), or as
  Annunciators and alarms setpoints
              requiring the establishment of appropriate and adequate goals and corrective
  The inspectors also verified that licensee personnel identified and implemented any needed corrective actions associated with the surveillance testing.
              actions for systems classified as not having adequate performance, as described
  June 10, 2012, Spent
              in 10 CFR 50.65(a)(1)
fuel pool pump B inservice testing  March 19, 2012, Main
    The inspectors assessed performance issues with respect to the reliability, availability,
steam isolation valve inservice testing  June 20, 2012, STS BB
    and condition monitoring of the system. In addition, the inspectors verified maintenance
-006, reactor coolant system leak rate calculation
    effectiveness issues were entered into the corrective action program with the appropriate
  June 21, 2012, Containment
    significance characterization. Specific documents reviewed during this inspection are
spray pump B inservice testing
    listed in the attachment.
  June 27, 2012, Residual
    These activities constitute completion of two quarterly maintenance effectiveness
heat removal pump A inservice testing  June 28, 2012, TMP 11
    samples as defined in Inspection Procedure 71111.12-05.
-013, Reactor
                                              - 11 -                          Enclosure
coolant system to emergency core cooling system check valve leak test  Specific documents reviewed during this inspection are listed in the attachment.
 
  These activities constitute completion of six surveillance testing inspection sample
  b. Findings
s as defined in Inspection Procedure
    No findings were identified.
71111.22-05.  b. Findings No findings were identified.
1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)
 
2. RADIATION SAFETY
  Cornerstone:  Occupational and Public Radiation Safety
  2RS05 Radiation Monitoring Instrumentation (71124.05)
   a. Inspection Scope
   a. Inspection Scope
  This area was inspected to verify the licensee is assuring the accuracy and operability of radiation monitoring instruments that are used to: (1) monitor areas, materials, and workers to ensure a radiologically safe work environment
    The inspectors reviewed licensee personnel's evaluation and management of plant risk
and (2) detect and quantify radioactive process streams and effluent releases.  The inspectors used the requirements in 10 CFR Part 20, the technical specifications, and the licensee's procedures required by technical specifications as criteria for determining compliance. During the inspection, the inspectors interviewed licensee personnel, performed walkdowns of various portions of the plant, and reviewed the following items:
    for the maintenance and emergent work activities affecting risk-significant and safety-
 
    related equipment listed below to verify that the appropriate risk assessments were
  - 19 - Enclosure  Selected plant configurations and alignments of process, post
    performed prior to removing equipment for work:
-accident, and effluent monitors with descriptions
          *  April 10 and 15, 2012, NK02 DC bus voltage and current fluctuations
in the USAR and the offsite dose calculation manual    Select instrumentation, including effluent monitoring instrument, portable survey instruments, area radiation monitors, continuous air monitors, personnel contamination monitors, portal monitors, and small article monitors to examine their configurations and source checks
    The inspectors selected these activities based on potential risk significance relative to
  Calibration and testing of process and effluent monitors, laboratory instrumentation, whole body counters, post-accident monitoring instrumentation, portal monitors , personnel contamination monitors , small article monitors , portable survey instruments, area radiation monitors, electronic dosimetry, ai
    the Reactor Safety Cornerstones. As applicable for each activity, the inspectors verified
r samplers, continuous air monitors
    that licensee personnel performed risk assessments as required by 10 CFR 50.65(a)(4)
  Audits, self
    and that the assessments were accurate and complete. When licensee personnel
-assessments, and corrective action documents related to radiation monitoring instrumentation
    performed emergent work, the inspectors verified that the licensee personnel promptly
since the last inspection
    assessed and managed plant risk. The inspectors reviewed the scope of maintenance
  Specific documents reviewed during this inspection are listed in the attachment.
    work, discussed the results of the assessment with the licensee's probabilistic risk
These activities constitute completion of the one required sample as defined in Inspection Procedure
    analyst or shift technical advisor, and verified plant conditions were consistent with the
71124.05-05. b. Findings No findings were identified.
    risk assessment. The inspectors also reviewed the technical specification requirements
  2RS06 Radioactive Gaseous and Liquid Effluent Treatment (71124.06)
    and inspected portions of redundant safety systems, when applicable, to verify risk
    analysis assumptions were valid and applicable requirements were met. Specific
    documents reviewed during this inspection are listed in the attachment.
    These activities constitute completion of one maintenance risk assessments and
    emergent work control inspection sample as defined in Inspection
    Procedure 71111.13-05.
  b. Findings
    No findings were identified.
1R15 Operability Evaluations and Functionality Assessments (71111.15)
   a. Inspection Scope
   a. Inspection Scope
  This area was inspected to: (1)
    The inspectors reviewed the following issues:
ensure the gaseous and liquid effluent processing systems are maintained so radiological discharges are properly mitigated, monitored,  
          *  April 13, 2012, Chemical and volume control system alternate charging line
and evaluated with respect to public exposure; (2) ensure abnormal radioactive gaseous or liquid discharges and conditions, when effluent radiation monitors are out
              check valves BBV8379A and BBV8379B potential stud degradation
-of-service, are controlled in accordance with the applicable regulatory requirements and licensee procedures; (3) verify the licensee
          *  April 18, 2012, Flood door operability in Auxiliary Building
=s quality control program ensures the radioactive effluent sampling and analysis requirements are satisfied so discharges of radioactive materials are adequately quantified and evaluated; and (4) verify the adequacy of public dose projections resulting from radioactive effluent discharges.  The inspectors used
          *  May 2, 2012, Operator Manual Actions for control room ventilation damper GKD-
the requirements in 10 CFR Part 20; 10 CFR Part 50, Appendices A and I; 40 CFR Part 190; the offsite dose calculation
              181
manual, and licensee procedures required by the
                                            - 12 -                           Enclosure
technical specifications as criteria for determining compliance.  The inspectors interviewed licensee personnel and reviewed and/or observed the following items:
 
  Radiological effluent release reports since the previous inspection and
        *    May 23, 2012, Refueling water storage tank valve BNV-11 manual actions during
reports related to the effluent program issued since the previous inspection, if any
              sump recirculation
 
        *   June 16, 2012, Vital Switchgear room temperatures after loss of train B air
  - 20 - Enclosure Effluent program implementing procedures, including sampling, monitor setpoint determinations and dose calculations
              conditioning unit
   Equipment configuration and flow paths of selected gaseous and liquid discharge system components, filtered ventilation system material condition, and significant changes to their effluent release points, if any, and associated 10 CFR 50.59 reviews  Selected portions of the routine processing and discharge of radioactive gaseous and liquid effluent s (including sample collection and analysis)
        *   January 24 and February 13, 2012, residual heat removal transients following
    Controls used to ensure representative sampling and appropriate compensatory
              non-vital power loss with normal service water running in Mode 5
sampling   Results of the inter
    The inspectors selected these potential operability issues based on the risk significance
-laboratory comparison program
    of the associated components and systems. The inspectors evaluated the technical
  Effluent stack flow rates
    adequacy of the evaluations to ensure that technical specification operability was
    Surveillance test results
    properly justified and the subject component or system remained available such that no
of technical specification
    unrecognized increase in risk occurred. The inspectors compared the operability and
-required ventilation effluent discharge systems  since the previous
    design criteria in the appropriate sections of the technical specifications and USAR to
inspection  Significant changes in reported dose values, if any  A selection of radioactive liquid and gaseous waste discharge permits
    the licensee personnels evaluations to determine whether the components or systems
  Part 61 analyses and methods used to determine which isotopes are included in the source term
    were operable. Where compensatory measures were required to maintain operability,
  Offsite dose calculation manual changes, if any
    the inspectors determined whether the measures in place would function as intended
  Meteorological dispersion and deposition factors
    and were properly controlled. The inspectors determined, where appropriate,
  Latest land use censu
    compliance with bounding limitations associated with the evaluations. Additionally, the
s    Records of abnormal gaseous or liquid tank discharges, if any
    inspectors also reviewed a sampling of corrective action documents to verify that the
  Groundwater monitoring results
    licensee was identifying and correcting any deficiencies associated with operability
  Changes to the licensee
    evaluations. Specific documents reviewed during this inspection are listed in the
's written program for indentifying and controlling contaminated spills/leaks to groundwater, if any
    attachment.
  Identified leakage or spill events and entries made into 10 CFR 50.75 (g)
    These activities constitute completion of six operability evaluation inspection samples as
records, if any, and associated evaluations of the extent of the contamination and the radiological source term
    defined in Inspection Procedure 71111.15-05.
  Offsite notifications
   b. Findings
, and reports
    No findings were identified.
of events associated with spills, leaks, or groundwater monitoring results, if any 
1R18 Plant Modifications (71111.18)
  - 21 - Enclosure  Audits, self
    Temporary Modifications
-assessments, reports, and corrective action documents related to radioactive gaseous and liquid effluent treatment
since the last inspection
  Specific documents reviewed during this inspection are listed in the attachment.
  These activities constitute completion of the one required sample , as defined in Inspection Procedure
7112 4.0 6-05.  b. Findings No findings were identified.
  2RS07 Radiological Environmental Monitoring Program (71124.07)
   a. Inspection Scope
   a. Inspection Scope
  This area was inspected to:
    To verify that the safety functions of important safety systems were not degraded, the
  (1) ensure that the radiological environmental monitoring program verifies the impact of radioactive effluent releases to the environment and sufficiently validates the integrity of the radioactive gaseous and liquid effluent release program; (2) verify that the radiological environmental monitoring program
    inspectors reviewed the temporary modification for leak seal repair of steam generator
is implemented consistent with the licensee's technical specifications and/or offsite dose calculation manual, and to validate that the radioactive effl
    tube sheet drain valve BMV0037.
uent release program meets the design objective contained in Appendix I to 10 CFR Part 50; and
    The inspectors reviewed the temporary modification and the associated safety-
(3) ensure that the radiological environmental monitoring program
    evaluation screening against the system design bases documentation, including the
monitors non
    USAR and the technical specifications, and verified that the modification did not
-effluent exposure pathways, is based on sound principles and assumptions, and validates that doses to members of the public are within the dose limits of 10 CFR Part 20 and  
    adversely affect the system operability/availability. The inspectors also verified that the
40 CFR Part 190 , as applicable.
    installation and restoration were consistent with the modification documents and that
  The inspectors reviewed and/or observed the following items:  Annual environmental monitoring reports and offsite dose calculation manual
    configuration control was adequate. Additionally, the inspectors verified that the
    Selected air sampling and thermoluminescence dosimeter monitoring stations
                                              - 13 -                            Enclosure
 
 
Collection and preparation of environmental samples
  temporary modification was identified on control room drawings, appropriate tags were
 
  placed on the affected equipment, and licensee personnel evaluated the combined
Operability, calibration, and maintenance of meteorological instruments
  effects on mitigating systems and the integrity of radiological barriers.
 
  These activities constitute completion of one sample for temporary plant modifications as
Selected event s documented in the annual environmental monitoring report which involved a missed sample, inoperable sampler, lost thermoluminescence dosimeter, or anomalous measurement
  defined in Inspection Procedure 71111.18-05.
   Selected structures, systems, or components that may contain licensed material
b. Findings
and has a credible mechanism for licensed material to reach ground water
  Introduction. The inspectors identified a Green non-cited violation of 10 CFR Part 50,
   Records required by 10 CFR 50.75(g)
  Appendix B, Criterion V, Instructions, Procedures, and Drawings, for a work order that
    
  did not accomplish a leak seal repair in accordance with its engineering evaluation.
  - 22 - Enclosure Significant changes made by the licensee to the offsite dose calculation manual as the result of changes to the land census or sampler station modifications since the last inspection
  Description. Valve BMV0037 is a 2-inch safety-related ASME Code Class 2 valve that
  Calibration and maintenance records for selected air samplers, composite water samplers, and environmental sample radiation measurement instrumentation
  isolates the steam generator B tube sheet drain. This diaphragm type valve is not
  Interlaboratory comparison program results
  required to change position but it is required to be a pressure boundary for the
 
  secondary side of the steam generator. This safety-related quality valve is normally
Audits, self
  closed and cannot be isolated from the steam generator.
-assessments, reports, and corrective action documents related to the radiological environmental monitoring program since the last inspection
  On September 9, 2010, Wolf Creek experienced a leak at the body-to-bonnet joint for
  Specific documents reviewed during this inspection are listed in the attachment.
  valve BMV0037. Wolf Creek engineering utilized a previously approved a leak seal
  These activities constitute completion of the one required sample as defined in Inspection Procedure
  repair using configuration change package 9385. Change package 13482 re-approved
71124.0 7-05. b. Findings  No findings were identified.
  change package 9385 for use. This change package approved drilling injection ports
  2RS08 Radioactive Solid Waste Processing, and Radioactive Material Handling, Storage, and Transportation (71124.08)
  into the valve body. On September 30, 2010, Wolf Creek and its contractor drilled two
  injection ports 180 degrees apart on valve BMV0037 and injected leak sealant. From
  September 30, 2010, to November 30, 2011, valve BMV0037 leaked and was injected
  four times. On December 5, 2011, BMV0037 began leaking again and a third injection
  port was installed.
  The inspectors selected the inspection because the valve had leaked multiple times and
  was not replaced. The inspectors made a containment entry on March 27, 2012, and
  observed the sealant injection. The inspectors observed two injection ports drilled at
  angles to the valve body in close proximity to one another and a third approximately 180
  degrees on the other side of the valve body. Two of the injection ports were visually
  estimated at three quarters of an inch apart and at a shallow angle to the valve body.
  Valve BMV0037 was injected again on March 28, 2012, and May 8, 2012.
  The inspectors reviewed work order 10-333183-002 that was used on September 30,
  2010, to install the injection ports. The inspectors found no instructions in work
  order 10-333183-002 for the orientation of the drilling for the injection ports, although
  they were drilled 180 degrees apart. Step 1.7.5 of work order 10-333183-002 stated that
  the activity was not to exceed three injection ports. The inspectors reviewed work
  order 11-346576-006, which installed a third injection port on December 10, 2011,
   adjacent to one of the existing injection ports. The inspectors noted that Step 1.8.4 of
  work order 11-346576-006 allowed the location of the third injection port to be
   determined by the vendor technician, and also noted that the third injection port was not
   installed in accordance with change package 9385.
                                          - 14 -                             Enclosure
 
The inspectors concluded that, despite repeated re-injections, Wolf Creek did not
exceed the evaluated limits for the amount of sealant allowed to be injected. However,
the inspectors noted that Wolf Creeks leak seal process did not require a valve with a
temporary leak seal repair to be replaced at the next outage, and it did not include a
caution that cooling down a hot system was likely to cause changes in the sealant
properties and result in another leak. The inspectors questioned why the valve was not
replaced during the previous refueling outage or the forced outage and were told that
Wolf Creek had had difficulty locating a replacement valve.
The inspectors reviewed configuration change packages 13482 and 9385. The
inspectors noted that configuration change package 9385 stated that three injection
ports shall be installed 120 degrees apart around the circumference of the valve body.
The holes for those injection ports were said not to require reinforcement because ASME
Code Section III, NC-3332.1 does not require reinforcement since the injection ports are
less than 2-inch nominal pipe size. ASME Code Section III, article NC-3300 is for
pressure vessels. The inspectors, with assistance from the Office of Nuclear Reactor
Regulation, determined that the use of article NC-3300 was reasonable, but the
application of article NC-3332.1 was not appropriate for multiple openings in a valve
body. The inspectors questioned if the reinforcement requirements of article NC-3330
were met. Wolf Creek subsequently evaluated the article NC-3330 reinforcement criteria
using dimensions reasonably estimated from a photo and the manufacturers valve
drawing. The inspectors concluded that the evaluation did not include the angles of the
injection ports. Drilling the injection ports at an angle other than 90 degrees (to the valve
body) results in a deeper hole to reach the body-to-bonnet threaded joint (the area
where the sealant was injected). This required more surrounding re-enforcement
material. The inspectors again questioned the loss of material, this time due to the
additional material lost to the injection port angles. Wolf Creek subsequently took actual
measurements during a containment entry and re-performed the ASME Code evaluation.
The evaluation considered the angled injection ports to be oval shaped holes through
the wall of the valve body per article NC-3331(a). This increased the amount of material
required for reinforcement. The inspectors reviewed the calculation and concluded that
the reinforcement requirements were met.
Analysis. The failure to ensure that the configuration of a safety-related steam generator
blowdown valve was controlled in accordance with the approved engineering change
package during leak seal activities is a performance deficiency. This finding was more
than minor because it impacted the procedure quality attribute of the Initiating Events
Cornerstone, and it affected the objective to limit the likelihood of those events that upset
plant stability and challenge critical safety functions during shutdown as well as power
operations. Using Inspection Manual Chapter 0609, Appendix A, The Significance
Determination Process (SDP) for Findings At-Power, this finding was determined to be
of very low safety significance because an evaluation after the modification was able to
demonstrate structural integrity. Therefore, the finding does not contribute to both the
likelihood of a reactor trip and the likelihood that mitigation equipment will not be
available. The inspectors identified the cause of the finding had a in the human
performance crosscutting aspect in the area of resources. Specifically, the licensee did
not ensure that the work order instructions were sufficiently complete, accurate and
reflected up-to-date design documentation sufficient to control plant configuration in
accordance with design [H.2.c.]
                                          - 15 -                            Enclosure
 
    Enforcement. Title 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures,
    and Drawings, requires, in part, that activities affecting quality shall be prescribed by
    documented instructions, procedures, or drawings, of a type appropriate to the
    circumstances and shall be accomplished in accordance with these instructions,
    procedures, or drawings. Instructions, procedures, or drawings shall include acceptance
    criteria for determining that activities have been satisfactorily accomplished. Wolf Creek
    configuration change package 9385 allowed up to three injection ports 120 degrees
    apart on the valve body. Contrary to the above, on September 30, 2010, the licensee
    performed an activity affecting quality using documented instructions that were not
    appropriate to the circumstances. Work order 10-333183-002 contained no instructions
    for the modification of the safety-related valve BMV0037 by installing injection ports.
    Specifically, there were no instructions or acceptance criteria for injection port positioning
    or orientation, even though the position and orientation to the drilled holes affect the
    structural integrity of the valve body. Because this issue was determined to be of very
    low safety significance (Green) and was entered into the licensees corrective action
    program as condition report 52992, this violation is being treated as a non-cited violation
    in accordance with Section VI.A.1 of the NRC Enforcement Policy: NCV
    05000482/2012003-02, Incorrect Leak Seal Injection Port Installation.
1R19 Post Maintenance Testing (71111.19)
   a. Inspection Scope
   a. Inspection Scope
  This area was inspected to verify the effectiveness of the licensee
    The inspectors reviewed the following postmaintenance activities to verify that
=s programs for processing, handling, storage, and transportation of radioactive material.  The inspectors used the requirements of 10
    procedures and test activities were adequate to ensure system operability and functional
CFR Parts 20, 61, and 71 and Department of Transportation regulations contained in 49 CFR Parts
    capability:
171-180 for determining compliance.
          *  May 31, 2012, Vital switchgear cooler SGK05B after compressor replacement
The inspectors interviewed licensee personnel and reviewed the following items:  The solid radioactive waste system description, process control program, and the scope of the licensee
          *  June 21, 2012, Containment spray room cooler after inspection
=s audit program
          *  June 18-25, 2012, Over-temperature delta-temperature circuit card replacements
  Control of radioactive waste storage areas including container labeling/marking and monitoring containers for deformation or signs of waste decomposition
    The inspectors selected these activities based upon the structure, system, or
  Changes to the liquid and solid waste processing system
    component's ability to affect risk. The inspectors evaluated these activities for the
configuration including a review of waste processing equipment that is not operational or abandoned in place  Radio-chemical sample analysis results for radioactive waste streams and use of scaling factors and calculations to account for difficult
    following (as applicable):
-to-measure radionuclides
          *  The effect of testing on the plant had been adequately addressed; testing was
  Processes for waste classification including use of scaling factors and  
              adequate for the maintenance performed
10 CFR Part 61 analysis
          *  Acceptance criteria were clear and demonstrated operational readiness; test
 
              instrumentation was appropriate
  - 23 - Enclosure  Shipment packaging, surveying, labeling, marking, placarding, vehicle checking, driver instructing, and preparation of the disposal manifest
    The inspectors evaluated the activities against the technical specifications, the USAR,
  Audits, self
    10 CFR Part 50 requirements, licensee procedures, and various NRC generic
-assessments, reports, and corrective action reports radioactive solid waste processing, and radioactive material handling, storage, and
    communications to ensure that the test results adequately ensured that the equipment
transportation
    met the licensing basis and design requirements. In addition, the inspectors reviewed
  performed since the last inspection
    corrective action documents associated with postmaintenance tests to determine
  Specific documents reviewed during this inspection are listed in the attachment.
    whether the licensee was identifying problems and entering them in the corrective action
  These activities constitute completion of the one required sample as defined in Inspection Procedure
    program and that the problems were being corrected commensurate with their
71124.08-05. b. Findings No findings were identified.
                                              - 16 -                            Enclosure
   4. OTHER ACTIVITIES
 
Cornerstones:  Initiating Events, Mitigating Systems, Barrier Integrity, Emergency Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Physical Protection
    importance to safety. Specific documents reviewed during this inspection are listed in
4OA1 Performance Indicator Verification (71151)
    the attachment.
.1 Data Submission Issue
    These activities constitute completion of three postmaintenance testing inspection
a. Inspection Scope
    samples as defined in Inspection Procedure 71111.19-05.
The inspectors performed a review of the performance indicator data submitted by the licensee for the first Quarter 20 12 performance indicators
  b. Findings
for any obvious inconsistencies prior to its public release in accordance with Inspection Manual
    No findings were identified.
Chapter 0608, "Performance Indicator Program."
1R22 Surveillance Testing (71111.22)
    
   a. Inspection Scope
This review was performed as part of the inspectors' normal plant status activities and, as such, did not constitute a separate inspection sample.
    The inspectors reviewed the USAR, procedure requirements, and technical
   b. Findings No findings were identified.
    specifications to ensure that the surveillance activities listed below demonstrated that the
   .2 Reactor Coolant System Specific Activity (BI01)
    systems, structures, and/or components tested were capable of performing their
a. Inspection Scope
    intended safety functions. The inspectors either witnessed or reviewed test data to
The inspectors sampled licensee submittals for the reactor coolant system specific activity performance
    verify that the significant surveillance test attributes were adequate to address the
indicator for the period from the second quarter 20 12 through the first quarter 20 12.  To determine the accuracy of the performance indicator data reported during those periods, the inspectors used definitions and guidance contained in NEI Document 99
    following:
-02, "Regulatory Assessment Performance Indicator Guideline," Revision
          *   Preconditioning
6.    
          *  Evaluation of testing impact on the plant
   - 24 - Enclosure The inspectors reviewed the licensee's reactor coolant system chemistry samples, technical specification requirements, issue reports, event reports
          *  Acceptance criteria
, and NRC integrated inspection reports for the period of April 1, 201
          *   Test equipment
1 , through March 30, 2012
          *   Procedures
, to validate the accuracy of the submittals.  The inspectors also reviewed the licensee's issue report database to determine if any problems had been identified with the performance indicator data collected or transmitted for this indicator and
          *  Jumper/lifted lead controls
none were identified.  
          *  Test data
These activities
          *  Testing frequency and method demonstrated technical specification operability
constitute completion of  
          *  Test equipment removal
one reactor coolant system specific activity sample as defined in Inspection Procedure
          *  Restoration of plant systems
71151-05. b. Findings No findings were identified.
          *  Fulfillment of ASME Code requirements
  .3 Reactor Coolant System Leakage (BI02)
          *  Updating of performance indicator data
a. Inspection Scope
          *  Engineering evaluations, root causes, and bases for returning tested systems,
The inspectors sampled licensee submittals for the reactor coolant system leakage
              structures, and components not meeting the test acceptance criteria were correct
performance indicator for the period from the
                                              - 17 -                          Enclosure
second quarter 20 11 through the first quarter 20 12.  To determine the accuracy of the performance indicator data reported during those periods, the inspectors used definitions and guidance contained in NEI Document 99
 
-02, "Regulatory Assessment Performance Indicator Guideline," Revision
          *   Reference setting data
6.  The inspectors reviewed the licensee's operator logs; reactor coolant system leakage tracking data, issue reports, event reports
          *   Annunciators and alarms setpoints
, and NRC integrated inspection reports for the period of April 1, 2011
      The inspectors also verified that licensee personnel identified and implemented any
, through March 31, 2012
      needed corrective actions associated with the surveillance testing.
, to validate the accuracy of the submittals.  The inspectors also reviewed the licensee's issue report database to determine if any problems had been identified with the performance indicator data collected or transmitted for this indicator and none were identified.  Specific documents
          *  June 10, 2012, Spent fuel pool pump B inservice testing
reviewed are described in the attachment to this report.
          *  March 19, 2012, Main steam isolation valve inservice testing
   These activities constitute completion of one reactor coolant system leakage sample as defined in Inspection Procedure
          *  June 20, 2012, STS BB-006, reactor coolant system leak rate calculation
71151-05.  b. Findings No findings were identified.
          *  June 21, 2012, Containment spray pump B inservice testing
   4OA2 Problem Identification and Resolution
          *  June 27, 2012, Residual heat removal pump A inservice testing
(71152) .1 Routine Review of Identification and Resolution of Problems
          *  June 28, 2012, TMP 11-013, Reactor coolant system to emergency core cooling
a. Inspection Scope
              system check valve leak test
As part of the various baseline inspection procedures discussed in previous sections of
      Specific documents reviewed during this inspection are listed in the attachment.
this report, the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify that they were being entered into the licensee's corrective action program at an appropriate threshold, that adequate attention was being given to timely corrective actions, and that adverse trends were identified and addressed.  The inspectors reviewed attributes that included the
      These activities constitute completion of six surveillance testing inspection samples as
  complete and accurate 
      defined in Inspection Procedure 71111.22-05.
  - 25 - Enclosure identification of the problem; the timely correction, commensurate with the safety significance; the evaluation and disposition of performance issues, generic implications, common causes, contributing factors, root causes, extent of condition reviews, and previous occurrences reviews; and the classification, prioritization, focus, and timeliness of corrective actions.  Minor issues entered into the licensee's corrective action program
  b. Findings
because of the inspectors' observations are included in the attached list of documents reviewed. 
      No findings were identified.
These routine reviews for the identification and resolution of problems did not constitute any additional inspection samples. Instead, by procedure, they were considered an
2.   RADIATION SAFETY
integral part of the inspections performed during the quarter and documented in Section 1 of this report.
      Cornerstone: Occupational and Public Radiation Safety
  b. Findings No findings were identified.
2RS05 Radiation Monitoring Instrumentation (71124.05)
  .2 Daily Corrective Action Program Reviews
  a. Inspection Scope
a. Inspection Scope
      This area was inspected to verify the licensee is assuring the accuracy and operability of
In order to assist with the identification of repetitive equipment failures and specific human performance issues for follow
      radiation monitoring instruments that are used to: (1) monitor areas, materials, and
-up, the inspectors performed a daily screening of items entered into the licensee's corrective action program.  The inspectors
      workers to ensure a radiologically safe work environment and (2) detect and quantify
accomplished this through review of the station's daily corrective action documents. The inspectors performed these daily reviews as part of their daily plant status monitoring activities and, as such, did not constitute any separate inspection samples.
      radioactive process streams and effluent releases. The inspectors used the
  b. Findings No findings were identified.
      requirements in 10 CFR Part 20, the technical specifications, and the licensees
  .3 Selected Issue Follow
      procedures required by technical specifications as criteria for determining compliance.
-up Inspection
      During the inspection, the inspectors interviewed licensee personnel, performed
  a. Inspection Scope
      walkdowns of various portions of the plant, and reviewed the following items:
The inspectors reviewed the causes and corrective actions for failure of
                                              - 18 -                            Enclosure
contain ment penetration assembly 274 electrical module
 
AThis resulted in the loss of the pressurizer backup group 1 heaters on March 18, 2012.
          *  Selected plant configurations and alignments of process, post-accident, and
  The inspectors reviewed the vendor hardware failure analysis report stating that a high resistance connection developed in the butt splice inside the epoxy seal.
              effluent monitors with descriptions in the USAR and the offsite dose calculation
  The inspectors reviewed Wolf Creek's apparent cause and extent of condition corrective actions and found that Wolf Creek has visually inspected other similar penetrations. Wolf Creek also has corrective actions perform thermography while penetrations are energized in order to detect failure at an earlier stage.
              manual
  The inspectors compared Wolf Creek's evaluation with guidance from the EPRI on containment building electrical penetration modules and did not find any missing maintenance activities that may have prevented the loss of the pressurizer backup group 1 heaters. Most degradation related to aging of the rubber seals in  
          *  Select instrumentation, including effluent monitoring instrument, portable survey
  - 26 - Enclosure contact with the inner and outer surfaces of containment and not the electrical conductors.
              instruments, area radiation monitors, continuous air monitors, personnel
 
              contamination monitors, portal monitors, and small article monitors to examine
These activities constitute completion of
              their configurations and source checks
one in-depth problem identification and resolution sample as defined in Inspection Procedure
          *   Calibration and testing of process and effluent monitors, laboratory
  71152-05.  b. Findings  No findings were identified.
              instrumentation, whole body counters, post-accident monitoring instrumentation,
  4OA3 Followup of Events and Notices of Enforcement Discretion (71153)
              portal monitors, personnel contamination monitors, small article monitors,
   (Closed) Licensee Event Report
              portable survey instruments, area radiation monitors, electronic dosimetry, air
0 50 00 482/2012003-00, Train
              samplers, continuous air monitors
B ECCS Inoperable Due to Damaged Watertight Containment Spray Pump Door Seal
          *   Audits, self-assessments, and corrective action documents related to radiation
  On April 17, 2012, at
              monitoring instrumentation since the last inspection
2: 53 p.m., the watertight door seal for the train
      Specific documents reviewed during this inspection are listed in the attachment.
B containment
      These activities constitute completion of the one required sample as defined in
spray pump room was determined to be nonfunctional and the equipment supported by the door was inoperable.  
      Inspection Procedure 71124.05-05.
The equipment supported by the door is the train
  b.  Findings
B residual heat removal pump
      No findings were identified.
  and the train
2RS06 Radioactive Gaseous and Liquid Effluent Treatment (71124.06)
B containment spray pump. The door was repaired on April 18, 2012 , at 2: 48 p.mThe watertight seal was replaced, welding was performed on the knife
  a. Inspection Scope
-edge of the door and the door lugs were tightened.
      This area was inspected to: (1) ensure the gaseous and liquid effluent processing
  The apparent cause of
      systems are maintained so radiological discharges are properly mitigated, monitored,
this condition was a less than adequate preventive maintenance to identify potentially deficient door seals.
      and evaluated with respect to public exposure; (2) ensure abnormal radioactive gaseous
  This event is reportable under 10 CFR 50.73(a)(2)(i)(B) as an operation or condition prohibited by Technical Specifications 3.5.2, 3.5.3, 3.6.6, and  
      or liquid discharges and conditions, when effluent radiation monitors are out-of-service,
Limiting Condition of Operation (LCO) 3.0.4.
      are controlled in accordance with the applicable regulatory requirements and licensee
  This condition is also reportable pursuant
      procedures; (3) verify the licensee=s quality control program ensures the radioactive
10 CFR 50.73(a)(2)(v) as an event or condition that could have prevented the fulfillment of a safety function because the opposite train was out of service several
      effluent sampling and analysis requirements are satisfied so discharges of radioactive
times while the seal was degraded
      materials are adequately quantified and evaluated; and (4) verify the adequacy of public
      dose projections resulting from radioactive effluent discharges. The inspectors used the
At the time of this
      requirements in 10 CFR Part 20; 10 CFR Part 50, Appendices A and I; 40 CFR Part 190;
licensee event report issued on June 18, 2012
      the offsite dose calculation manual, and licensee procedures required by the technical
, the inspectors had already inspected this event under baseline inspection procedure 71111.06.  The results of that inspection can be found in section 1R06 of this report
      specifications as criteria for determining compliance. The inspectors interviewed
  These activities constitute completion of
      licensee personnel and reviewed and/or observed the following items:
one event follow
          *  Radiological effluent release reports since the previous inspection and reports
-up sample as defined in Inspection Procedure
              related to the effluent program issued since the previous inspection, if any
71151-05.  b. Findings  No findings were identified.
                                              - 19 -                            Enclosure
  4OA5 Other Activities
 
Assessment of Corrective Action to Address
  * Effluent program implementing procedures, including sampling, monitor setpoint
Substantive Cross
  determinations and dose calculations
cutting Issues P.1.a, P.1.c, and P.1.d
  * Equipment configuration and flow paths of selected gaseous and liquid discharge
  system components, filtered ventilation system material condition, and significant
  changes to their effluent release points, if any, and associated 10 CFR 50.59
  reviews
  * Selected portions of the routine processing and discharge of radioactive gaseous
  and liquid effluents (including sample collection and analysis)
  * Controls used to ensure representative sampling and appropriate compensatory
  sampling
* Results of the inter-laboratory comparison program
* Effluent stack flow rates
* Surveillance test results of technical specification-required ventilation effluent
  discharge systems since the previous inspection
  * Significant changes in reported dose values, if any
* A selection of radioactive liquid and gaseous waste discharge permits
*  Part 61 analyses and methods used to determine which isotopes are included in
  the source term
*  Offsite dose calculation manual changes, if any
  * Meteorological dispersion and deposition factors
  * Latest land use census
* Records of abnormal gaseous or liquid tank discharges, if any
* Groundwater monitoring results
* Changes to the licensees written program for indentifying and controlling
  contaminated spills/leaks to groundwater, if any
  * Identified leakage or spill events and entries made into 10 CFR 50.75 (g)
  records, if any, and associated evaluations of the extent of the contamination and
   the radiological source term
* Offsite notifications, and reports of events associated with spills, leaks, or
  groundwater monitoring results, if any
                                    - 20 -                            Enclosure
 
          *  Audits, self-assessments, reports, and corrective action documents related to
              radioactive gaseous and liquid effluent treatment since the last inspection
      Specific documents reviewed during this inspection are listed in the attachment.
      These activities constitute completion of the one required sample, as defined in
      Inspection Procedure 71124.06-05.
  b. Findings
      No findings were identified.
2RS07 Radiological Environmental Monitoring Program (71124.07)
  aInspection Scope
      This area was inspected to: (1) ensure that the radiological environmental monitoring
      program verifies the impact of radioactive effluent releases to the environment and
      sufficiently validates the integrity of the radioactive gaseous and liquid effluent release
      program; (2) verify that the radiological environmental monitoring program is
      implemented consistent with the licensees technical specifications and/or offsite dose
      calculation manual, and to validate that the radioactive effluent release program meets
      the design objective contained in Appendix I to 10 CFR Part 50; and (3) ensure that the
      radiological environmental monitoring program monitors non-effluent exposure
      pathways, is based on sound principles and assumptions, and validates that doses to
      members of the public are within the dose limits of 10 CFR Part 20 and
      40 CFR Part 190, as applicable. The inspectors reviewed and/or observed the following
      items:
        *    Annual environmental monitoring reports and offsite dose calculation manual
        *    Selected air sampling and thermoluminescence dosimeter monitoring stations
        *    Collection and preparation of environmental samples
        *    Operability, calibration, and maintenance of meteorological instruments
        *    Selected events documented in the annual environmental monitoring report
              which involved a missed sample, inoperable sampler, lost thermoluminescence
              dosimeter, or anomalous measurement
        *    Selected structures, systems, or components that may contain licensed material
              and has a credible mechanism for licensed material to reach ground water
        *    Records required by 10 CFR 50.75(g)
                                                - 21 -                            Enclosure
 
        *  Significant changes made by the licensee to the offsite dose calculation manual
            as the result of changes to the land census or sampler station modifications since
            the last inspection
        *  Calibration and maintenance records for selected air samplers, composite water
            samplers, and environmental sample radiation measurement instrumentation
        *  Interlaboratory comparison program results
        *  Audits, self-assessments, reports, and corrective action documents related to the
            radiological environmental monitoring program since the last inspection
      Specific documents reviewed during this inspection are listed in the attachment.
      These activities constitute completion of the one required sample as defined in
      Inspection Procedure 71124.07-05.
  b.  Findings
      No findings were identified.
2RS08 Radioactive Solid Waste Processing, and Radioactive Material Handling, Storage,
      and Transportation (71124.08)
   a.  Inspection Scope
   a.  Inspection Scope
  Wolf Creek's letter dated May 7, 2012
      This area was inspected to verify the effectiveness of the licensee=s programs for
, informed the NRC of its readiness for inspection of substantive crosscutting issues P.1.a (problem identification), P.1.c (evaluation), and   
      processing, handling, storage, and transportation of radioactive material. The inspectors
  - 27 - Enclosure P.1.d (corrective action). From June 18 to 21, 2012, the inspectors gathered information to inform management's decision in the mid
      used the requirements of 10 CFR Parts 20, 61, and 71 and Department of
-2012 performance assessment. Consideration of possible closure of these substantive crosscutting issues will be a
      Transportation regulations contained in 49 CFR Parts 171-180 for determining
n NRC decision using information from this inspection, guidance in Inspection
      compliance. The inspectors interviewed licensee personnel and reviewed the following
Manual Chapter 0305, and the information discussed at a June 25, 2012
      items:
, public meeting.  The inspectors
          *  The solid radioactive waste system description, process control program, and the
review ed whether the substantive crosscutting issues
            scope of the licensee=s audit program
we re entered into the corrective action program
          * Control of radioactive waste storage areas including container labeling/marking
(CAP), the causes identified, the corrective actions identified to address
            and monitoring containers for deformation or signs of waste decomposition
those causes, the measures of effectiveness used by the licensee to monitor improvement, and actual data for those effectiveness reviews.
          * Changes to the liquid and solid waste processing system configuration including
  This inspection activity constituted one sample of semi
            a review of waste processing equipment that is not operational or abandoned in
-annual trend review under inspection procedure
            place
1152-05. b. Findings and Assessment
          *  Radio-chemical sample analysis results for radioactive waste streams and use of
No findings were identified.
            scaling factors and calculations to account for difficult-to-measure radionuclides
P.1.a entry into the CAP
          * Processes for waste classification including use of scaling factors and
  Wolf Creek addressed all P.1 substantive crosscutting issues in two main condition reports.  Condition report 23032 was a root cause evaluation completed for a second time in September 2010. Condition report 23032 was
            10 CFR Part 61 analysis
written in response to the problem identification and resolution and human performance substantive crosscutting issues
                                            - 22 -                            Enclosure
that led the site to Column III of the NRC's action matrix. Wolf Creek identified 63 corrective
 
actions that were to correct the problem identification and resolution problems. Condition report 34455 was also a root cause in response to the 2010 end of cycle assessment letter from the NRC. Condition report 34455 identified 27 corrective actions.
          *  Shipment packaging, surveying, labeling, marking, placarding, vehicle checking,
  The inspectors concluded that the licensee appropriately entered this issue into the CAP. P.1.a Causes
              driver instructing, and preparation of the disposal manifest
 
          *  Audits, self-assessments, reports, and corrective action reports radioactive solid
Root and apparent cause evaluation
              waste processing, and radioactive material handling, storage, and transportation
s were self-critical and they found a lack of management involvement and oversight in the corrective action program
              performed since the last inspection
over the last
      Specific documents reviewed during this inspection are listed in the attachment.
3 years.  These were the same causes identified for White performance indicators that the 95002 team
      These activities constitute completion of the one required sample as defined in
examined under condition report
      Inspection Procedure 71124.08-05.
23032. Condition report
  b. Findings
23032 had a second root cause that the station was over
      No findings were identified.
-confident in using the work controls process to manage critical equipment problems. Root cause 34455 ha
4.   OTHER ACTIVITIES
d a similar root cause of leadership not aligning station behaviors for timely problem identification and resolution. Root cause 34455 had a contributing cause that the station ha
      Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency
d inadequate training
      Preparedness, Public Radiation Safety, Occupational Radiation Safety, and
on the design and licensing basis which is inhibiting effective problem evaluation.
      Physical Protection
  Further, the root cause found that there was no regular training for certain personnel on the design basis or its controls. The inspectors concluded that the licensee effectively identified the causes
4OA1 Performance Indicator Verification (71151)
for this substantive crosscutting issue.
.1   Data Submission Issue
  P.1.a Corrective actions
  a. Inspection Scope
  The inspectors sampled corrective actions.  The previous large change in the corrective action program was to create the single point of entry
      The inspectors performed a review of the performance indicator data submitted by the
for all issues into the CAP.  This 
      licensee for the first Quarter 2012 performance indicators for any obvious
  - 28 - Enclosure eliminated the previous practice of
      inconsistencies prior to its public release in accordance with Inspection Manual
writing a work order for a problem
      Chapter 0608, Performance Indicator Program.
, and only allowed writing a condition report for each problem. While either method would work, the new method added working level and management level scrutiny to each condition report. The number of condition reports
      This review was performed as part of the inspectors normal plant status activities and,
written increased since this change, often with multiple condition reports on the same problem.
      as such, did not constitute a separate inspection sample.
This was implemented in January 2011, and was responsive to 23032 root cause number two.
  b. Findings
   The inspectors observed that an important programmatic change
      No findings were identified.
to the Wolf Creek corre ctive action software
.2    Reactor Coolant System Specific Activity (BI01)
was implemented
  a. Inspection Scope
on April 26, 2012. Although it does not appear to be directly linked to root cause 23032, a new department was formed which
      The inspectors sampled licensee submittals for the reactor coolant system specific
add ed more oversight to operability determinations and work control, which
      activity performance indicator for the period from the second quarter 2012 through the
wa s responsive the root causes.  Changes were made to track and evaluate degraded or
      first quarter 2012. To determine the accuracy of the performance indicator data reported
nonconforming conditions with a new department named
      during those periods, the inspectors used definitions and guidance contained in NEI
operations
      Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6.
work control.  The inspectors observed that the more recent immediate operability evaluations more closely tie the equipment requirements to the observed problems to confirm or refute operability or functionality (P.1.c).  Also, the new changes track each degraded condition
                                              - 23 -                          Enclosure
, and prevent equipment from being
 
returned to full service without
      The inspectors reviewed the licensees reactor coolant system chemistry samples,
a review of all corrective actions by a senior reactor operator. The inspectors concluded that
      technical specification requirements, issue reports, event reports, and NRC integrated
the added problem evaluation scrutiny
      inspection reports for the period of April 1, 2011, through March 30, 2012, to validate the
was consistent with the
      accuracy of the submittals. The inspectors also reviewed the licensees issue report
identified
      database to determine if any problems had been identified with the performance
causes. Although many methods of finding, evaluating, and fixing problems can work across the power reactor industry,
      indicator data collected or transmitted for this indicator and none were identified.
Wolf Creek chose to make CAP changes while instituting new guidance on the accountability of the CAP.
      These activities constitute completion of one reactor coolant system specific activity
  Based on a sampling review, the inspectors concluded that the corrective actions were appropriate to address the identified causes.
      sample as defined in Inspection Procedure 71151-05.
  P.1.a Corrective Action
  b. Findings
Effectiveness
      No findings were identified.
Measures  Wolf Creek internal metrics consist
.3    Reactor Coolant System Leakage (BI02)
ed of monitoring and trending the condition report initiation rate overall by the site and department. Identification of the issues by the NRC or other organizations, rather than by licensee personnel, negatively impact the metric. Condition report initiation rate
  a. Inspection Scope
metrics show
      The inspectors sampled licensee submittals for the reactor coolant system leakage
ed a steady increase with
      performance indicator for the period from the second quarter 2011 through the first
most departments
      quarter 2012. To determine the accuracy of the performance indicator data reported
having a high self identification rates in
      during those periods, the inspectors used definitions and guidance contained in NEI
Green with the exception of three in the  
      Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6.
R ed due to NRC and external organization identification
      The inspectors reviewed the licensees operator logs; reactor coolant system leakage
. The inspectors concluded that the licensee had developed reasonable effectiveness measures, and that those effectiveness measures demonstrated an improving trend
      tracking data, issue reports, event reports, and NRC integrated inspection reports for the
for the station, but that the red indicators reflected a continuation of a long standing trend in those areas
      period of April 1, 2011, through March 31, 2012, to validate the accuracy of the
. P.1.a Results
      submittals. The inspectors also reviewed the licensees issue report database to
 
      determine if any problems had been identified with the performance indicator data
The inspectors observed a low threshold for problems and condition reports. Personnel interviewed indicated no hesitation to initiate condition reports.  The inspectors observed several issues had two or more condition reports for the same problem.  Some problems were consolidated to one condition report while others were not. More than one person
      collected or transmitted for this indicator and none were identified. Specific documents
or work group may write a condition report for the same problem. Condition report problem statements for those condition reports were not always reconciled to ensur
      reviewed are described in the attachment to this report.
e that all aspects would be corrected. This was consistent with the observations of the biennial problem identification and resolution inspection documented in Inspection Report 2012007.
      These activities constitute completion of one reactor coolant system leakage sample as
  P.1.c Entry into the C AP 
      defined in Inspection Procedure 71151-05.
  - 29 - Enclosure  Wolf Creek addressed all P.1 substantive crosscutting issues in two main condition reports and one condition report from 2008. Condition report 23032 was a root cause evaluation completed for a second time in September 2010. Condition report 23032 was in response to the problem identification and resolution
   b. Findings
and human performance
      No findings were identified.
substantive crosscutting issues that led the site to being placed in Column III of the NRC's action matrix.  Wolf Creek identified 63 corrective actions that were to correct the
4OA2 Problem Identification and Resolution (71152)
problem identification and resolution problems.  Condition report
.1    Routine Review of Identification and Resolution of Problems
34455 also
  a. Inspection Scope
documented
      As part of the various baseline inspection procedures discussed in previous sections of
a root cause
      this report, the inspectors routinely reviewed issues during baseline inspection activities
analysis in response to the 2010 end of cycle assessment letter from the NRC. Condition report 34455 identified 27 corrective actions.  In the past,
      and plant status reviews to verify that they were being entered into the licensees
Wolf Creek
      corrective action program at an appropriate threshold, that adequate attention was being
also took action under condition report 2008-8810 for the P.1.c substantive cros scutting issue. The causes for 2008
      given to timely corrective actions, and that adverse trends were identified and
-8810 were nearly identical to the more recent root causes.
      addressed. The inspectors reviewed attributes that included the complete and accurate
  The inspectors concluded that the licensee appropriately entered this issue into the CAP.
                                              - 24 -                          Enclosure
  P.1.c Causes
 
 
      identification of the problem; the timely correction, commensurate with the safety
Root and apparent causes have been self
      significance; the evaluation and disposition of performance issues, generic implications,
-critical and they found a lack of management involvement and oversight in the corrective action program over the last
      common causes, contributing factors, root causes, extent of condition reviews, and
3 years. These were the same causes identified for White performance indicators that the 95002 team
      previous occurrences reviews; and the classification, prioritization, focus, and timeliness
examined under condition report
      of corrective actions. Minor issues entered into the licensees corrective action program
23032.  Root cause 34455 has a similar root cause of leadership not aligning station behaviors for timely problem identification and resolution.  Root Cause 34455 was written in March 2011 in response to the NRC's 2010 Assessment Letter, with the cause evaluation not completed until June 30, 2011. Root cause 34455 had a contributing cause of the station having poor training on the design and licensing basis which is inhibiting effective problem evaluation. A contributing cause was the over-reliance on the work control process to getting problems fixed.
      because of the inspectors observations are included in the attached list of documents
   Wolf Creek has repeatedly found that less than timely evaluations have contributed to delays in corrective actions for substantive cross cutting issues.  The inspectors concluded that the licensee effectively identified the causes for this substantive crosscutting issue.
      reviewed.
  P.1.c Corrective
      These routine reviews for the identification and resolution of problems did not constitute
Actions    
      any additional inspection samples. Instead, by procedure, they were considered an
The inspectors sampled corrective actions. The previous large change in the corrective action program was to create the single point of
      integral part of the inspections performed during the quarter and documented in
entry for all issues into the CAP. This eliminated the previous practice of writing a work order for a problem, and only allowed writing a condition report for each problem. While either method would work, the new method added working level and management level scrutiny to each condition report.  The licensee recent
      Section 1 of this report.
ly implemented
  b. Findings
an important programmatic change
      No findings were identified.
involving changes to the corrective action program software.  Although it does not appear to be directly linked to root cause 23032, a new department was formed which adds more oversight to operability determinations and work control, which is responsive the root causes.  Changes were made to track and evaluate degraded or non
.2    Daily Corrective Action Program Reviews
-conforming conditions with a new department named operations work contr
  a. Inspection Scope
ol. The inspectors observed that the more recent immediate operability evaluations more closely tie the  
      In order to assist with the identification of repetitive equipment failures and specific
equipment requirements to the observed problems to confirm or refute operability or functionality (P.1.c). Also, the new changes track each degraded condition and equipment cannot be returned to full service without review of all corrective actions by a
      human performance issues for follow-up, the inspectors performed a daily screening of
senior reactor operator (P.1.d).  The inspectors found the added problem evaluation 
      items entered into the licensees corrective action program. The inspectors
  - 30 - Enclosure scrutiny is consistent with the causes.  Although many methods of finding, evaluating, and fixing problems can work across the power reactor industry, Wolf Creek chose to make CAP changes while instituting new guidance on the accountability of the CAP. Most other corrective actions centered on recurring training for cause
      accomplished this through review of the stations daily corrective action documents.
evaluators and procedure changes to corrective action procedures, both directed at increasing the quality of condition report causal evaluations.
      The inspectors performed these daily reviews as part of their daily plant status
  P.1.c Corrective Action Effectiveness
      monitoring activities and, as such, did not constitute any separate inspection samples.
Measures.
  b. Findings
The licensee developed evaluation quality internal performance indications, including the results from
      No findings were identified.
corrective action review board
.3    Selected Issue Follow-up Inspection
and other challenge boards. T he results of these metrics
  a. Inspection Scope
were trending in a positive direction.  These quality metrics and oversight boards have undergone many changes in the last two years. The inspectors observed that the trends reflect the refueling and forced outages, which typically cause an increase in the number of evaluations needed
      The inspectors reviewed the causes and corrective actions for failure of containment
.  The operability evaluation metric up to May show ed a declining trend in quality
      penetration assembly 274 electrical module A. This resulted in the loss of the
over the last 6 months, though inspectors noted that Wolf Creek did not find any evaluations that failed to demonstrate operability.  Root
      pressurizer backup group 1 heaters on March 18, 2012. The inspectors reviewed the
and apparent cause evaluation completion timeliness goals show
      vendor hardware failure analysis report stating that a high resistance connection
ed an improving trend since October 2011, but are still
      developed in the butt splice inside the epoxy seal. The inspectors reviewed Wolf
R e d and do not show average completion times that are close to procedural limits.
      Creeks apparent cause and extent of condition corrective actions and found that Wolf
  The inspectors concluded that the licensee had developed reasonable effectiveness measures, although
      Creek has visually inspected other similar penetrations. Wolf Creek also has corrective
those effectiveness measures
      actions perform thermography while penetrations are energized in order to detect failure
failed to demonstrate sustained improvement
      at an earlier stage. The inspectors compared Wolf Creeks evaluation with guidance
.    P.1.c Results  Creating a single point of entry into the CAP was a significant change. The changes to improve tracking of degraded or non
      from the EPRI on containment building electrical penetration modules and did not find
-conforming conditions added some priority to fixing problems, but giving priority to these types of items is still not a formal process requirement.  Corrective actions are still largely prioritized in the work control process.  Most corrective actions have focused on improving condition report evaluation timeliness, providing evaluation methodology training (why tree, hazard
      any missing maintenance activities that may have prevented the loss of the pressurizer
-barrier-target, etc.), and improving coding and trending of causes.
      backup group 1 heaters. Most degradation related to aging of the rubber seals in
  The inspectors interviewed department corrective action coordinators and found that they had an active role in trending recurring problems in each department.  The inspectors saw this as a positive change but not directly related to evaluation quality.  Training on the plant design bases was positive and provided information on the overall regulatory framework, but did not include
                                                - 25 -                            Enclosure
specific requirements for the
 
trainees' systems or engineering discipline.  The inspectors saw improvement in the rejection of the root cause by the corrective action review board for the January 13, 2012, loss of offsite power, although not all rejections were captured by the station's metric.
    contact with the inner and outer surfaces of containment and not the electrical
  The inspectors reviewed Wolf Creek's comprehensive event safety
    conductors.
-significance evaluation which examined all the problems revealed during the January 13, 2012
    These activities constitute completion of one in-depth problem identification and
, loss of offsite power. Problem evaluation
    resolution sample as defined in Inspection Procedure 71152-05.
was stated as a contributing cause in that self-assessment. Corrective actions were deferred to an apparent cause evaluation stemming from a
  b. Findings
quality assurance audit that found the corrective action program marginally effective.
    No findings were identified.
  Corrective actions to that quality assurance assessment continued the trend of changes to cause method training and CAP procedure changes.  With 
4OA3 Followup of Events and Notices of Enforcement Discretion (71153)
  - 31 - Enclosure design basis training being a self
    (Closed) Licensee Event Report 05000482/2012003-00, Train B ECCS Inoperable Due
-identified weakness, inspectors observed that the number and high
    to Damaged Watertight Containment Spray Pump Door Seal
-level content of those training courses will challenge the adequacy of equipment specific problems, such as the leak seal repair in this report.
    On April 17, 2012, at 2:53 p.m., the watertight door seal for the train B containment spray
  The inspectors concluded that progress was being made toward implementing the corrective actions for this substantive cross
    pump room was determined to be nonfunctional and the equipment supported by the
-cutting issue, but that sustained improvement in the quality and timeliness of evaluations had not been demonstrated.
    door was inoperable. The equipment supported by the door is the train B residual heat
  P.1.d Entry into the C AP 
    removal pump and the train B containment spray pump. The door was repaired on
Wolf Creek addressed all P.1 substantive crosscutting issues in two main condition  
    April 18, 2012, at 2:48 p.m. The watertight seal was replaced, welding was performed
reports. Condition report 23032 was a root cause evaluation completed for a second time in September 2010.  Condition report 23032 was in response to the problem identification
    on the knife-edge of the door and the door lugs were tightened. The apparent cause of
and resolution
    this condition was a less than adequate preventive maintenance to identify potentially
and human performance
    deficient door seals. This event is reportable under 10 CFR 50.73(a)(2)(i)(B) as an
substantive crosscutting issues that led the site to Column III of the NRC's action matrix. Wolf Creek identified 63 corrective actions that were to correct the problem identification and resolution problems. Condition report 34455 was also a root cause
    operation or condition prohibited by Technical Specifications 3.5.2, 3.5.3, 3.6.6, and
in response to the 2010 end of cycle assessment letter from the NRC. Condition report 34455 identified 27 corrective actions.
    Limiting Condition of Operation (LCO) 3.0.4. This condition is also reportable pursuant
  The inspectors concluded that the licensee appropriately entered this issue into the CAP. P.1.d Causes
    10 CFR 50.73(a)(2)(v) as an event or condition that could have prevented the fulfillment
  Root and apparent c aus e evaluation
    of a safety function because the opposite train was out of service several times while the
s for this substantive cross
    seal was degraded.
-cutting issue were
    At the time of this licensee event report issued on June 18, 2012, the inspectors had
self-critical , and they documented
    already inspected this event under baseline inspection procedure 71111.06. The results
a lack of management involvement and oversight in the corrective action program over the last
    of that inspection can be found in section 1R06 of this report.
3 years. These are the
    These activities constitute completion of one event follow-up sample as defined in
same causes the 95002 team examined under condition report
    Inspection Procedure 71151-05.
23032.  Root cause 34455 ha
  b. Findings
d a similar root cause of leadership not aligning station behaviors for timely problem identification and resolution. Root cause 34455 had a contributing cause of the station having inadequate training on the design and licensing basis which
    No findings were identified.
was inhibiting effective problem evaluation.
4OA5 Other Activities
These causes are the same as those for the P.1.a and P.1.c substantive cross-cutting issues.  The previous large change in the corrective action program was to create the single point of entry
    Assessment of Corrective Action to Address Substantive Crosscutting Issues P.1.a,
  for all issues into the CAP. This eliminated the previous practice of writing a work order for a problem, and only allowed writing a condition report  
    P.1.c, and P.1.d
for each problem. While either method would work, the new method added working level and management level scrutiny to each condition report. The licensee recent
   a. Inspection Scope
l y implemented an
    Wolf Creeks letter dated May 7, 2012, informed the NRC of its readiness for inspection
important programmatic change
    of substantive crosscutting issues P.1.a (problem identification), P.1.c (evaluation), and
involving changes to the corrective action program software. Although it does not appear to be directly linked to root cause
                                            - 26 -                              Enclosure
23032, a new department was formed which adds more oversight to operability determinations and work control, which is responsive the root causes
 
  Changes were made to track and evaluate degraded or non
   P.1.d (corrective action). From June 18 to 21, 2012, the inspectors gathered information
-conforming conditions with a new department named
  to inform managements decision in the mid-2012 performance assessment.
operations
  Consideration of possible closure of these substantive crosscutting issues will be an
work control. The inspectors observed that the more recent immediate operability evaluations were more closely tie
  NRC decision using information from this inspection, guidance in Inspection Manual
d the equipment requirements to the observed problems in order to be able to confirm or refute operability or functionality. Also, the new changes track each degraded condition
  Chapter 0305, and the information discussed at a June 25, 2012, public meeting. The
, and required that equipment cannot be returned to full qualification without review of all corrective actions by a senior reactor operator. The inspectors concluded that
  inspectors reviewed whether the substantive crosscutting issues were entered into the
the increased problem evaluation scrutiny
  corrective action program (CAP), the causes identified, the corrective actions identified
wa s consistent with the causes. Although many methods of finding, evaluating, and fixing problems can work across the power reactor industry, Wolf Creek
  to address those causes, the measures of effectiveness used by the licensee to monitor
chose to make CAP changes while instituting new guidance on the accountability of the
  improvement, and actual data for those effectiveness reviews.
  - 32 - Enclosure CAP. The inspectors
  This inspection activity constituted one sample of semi-annual trend review under
concluded that the licensee effectively identified the causes for this substantive crosscutting issue.
  inspection procedure 1152-05.
  P.1.d Corrective Actions    The inspectors reviewed selected corrective actions that were most responsive to the root causes. Condition report 23032
b. Findings and Assessment
, action 2-9 , instituted on August 31, 2011
  No findings were identified.
, required the corrective actions review board review each issue coded as being a corrective action to prevent recurrence within 30 days of its closure. Separate from the root causes, the inspectors found other condition reports responding to NRC violations on annunciator
  P.1.a entry into the CAP
power supplies, emergency diesel loading, operability evaluations, and maintenance rule stating that there
  Wolf Creek addressed all P.1 substantive crosscutting issues in two main condition
was a need for continuing
  reports. Condition report 23032 was a root cause evaluation completed for a second
engineering training on standards for each of those issues. The inspectors reviewed training lesson plans for
  time in September 2010. Condition report 23032 was written in response to the problem
change package
  identification and resolution and human performance substantive crosscutting issues
continuing training [modifications], "Regulatory, Current Licensing Basis, And Design Basis ," and operability evaluation training for engineers and licensed operators.  The inspectors observed that the training
  that led the site to Column III of the NRCs action matrix. Wolf Creek identified 63
was conducted every 60 days.  Wolf Creek has instituted corrective action backlog measurement indicators as a corrective action.
  corrective actions that were to correct the problem identification and resolution problems.
  The inspectors noted that the act of trending is not a corrective action.
  Condition report 34455 was also a root cause in response to the 2010 end of cycle
  Those backlogs
  assessment letter from the NRC. Condition report 34455 identified 27 corrective actions.
remain high
  The inspectors concluded that the licensee appropriately entered this issue into the
, but have made some progress since the forced outage earlier this year. Engineering also ha d a significant backlog of over 5500 work orders
  CAP.
in May 2012. The corrective action backlog initiative plan require
  P.1.a Causes
d regular meetings for departments to drive a reduction in their backlog, but no other specific actions were developed, such as addressing actions by priorities.
  Root and apparent cause evaluations were self-critical and they found a lack of
  The inspectors also noted that there were a significant number of open actions to correct
  management involvement and oversight in the corrective action program over the last
NRC violations
  3 years. These were the same causes identified for White performance indicators that
, especially for scoping
  the 95002 team examined under condition report 23032. Condition report 23032 had a
of maintenance rule functions.
  second root cause that the station was over-confident in using the work controls process
  Based on a sampling review, the inspectors concluded that the corrective actions
  to manage critical equipment problems. Root cause 34455 had a similar root cause of
to address this substantive cross
  leadership not aligning station behaviors for timely problem identification and resolution.
-cutting aspect
  Root cause 34455 had a contributing cause that the station had inadequate training on
were partially appropriate to address the identified causes, but specific actions to ensure that CAP corrective actions were timely and effective were lacking
  the design and licensing basis which is inhibiting effective problem evaluation. Further,
. P.1.d Corrective Action
  the root cause found that there was no regular training for certain personnel on the
Effectiveness
  design basis or its controls. The inspectors concluded that the licensee effectively
Measures  Wolf Creek's effectiveness review for root cause condition report 23032 concluded that there was not sustained improvement
  identified the causes for this substantive crosscutting issue.
in ensuring that corrective actions were timely and effective  due to not meeting internal station metrics set for maintenance backlogs, repetitive maintenance rule functional failures, and two other failed effectiveness follow
  P.1.a Corrective actions
-ups.  The interim effectiveness follow-up for root cause condition report
  The inspectors sampled corrective actions. The previous large change in the corrective
34455 was met with the exception of one internal performance indicator for too great a ratio of  
  action program was to create the single point of entry for all issues into the CAP. This
NRC identified
                                          - 27 -                             Enclosure
to licensee identified findings. The inspectors observed that the identification credit is an NRC function and affects the indicator
 
, which may not be insightful
eliminated the previous practice of writing a work order for a problem, and only allowed
.  The conclusion of condition report 34455 interim effectiveness review stated that additional time was needed to increase the internal self
writing a condition report for each problem. While either method would work, the new
-identification metrics and that more time was needed.
method added working level and management level scrutiny to each condition report.
  Th is effectiveness review also gave credit for future expected improvement in the equipment performance index, a licensee metric, and which was
The number of condition reports written increased since this change, often with multiple
Yellow at the time of the inspection
condition reports on the same problem. This was implemented in January 2011, and
The final effectiveness follow
was responsive to 23032 root cause number two.
-up was scheduled to be completed by December 20, 2012. The non-cited violation
The inspectors observed that an important programmatic change to the Wolf Creek
closure effectiveness performance indicator
corrective action software was implemented on April 26, 2012. Although it does not
was R ed in January, February
appear to be directly linked to root cause 23032, a new department was formed which
, and March 2012.
added more oversight to operability determinations and work control, which was
Wolf Creek has written two condition reports
responsive the root causes. Changes were made to track and evaluate degraded or
on the non-cited violation
nonconforming conditions with a new department named operations work control. The
effectiveness performance indicator and the need to return it to
inspectors observed that the more recent immediate operability evaluations more closely
Green and are due to have formulated corrective actions by August 9, 2012.
tie the equipment requirements to the observed problems to confirm or refute operability
  The inspectors concluded that the licensee had developed 
or functionality (P.1.c). Also, the new changes track each degraded condition, and
  - 33 - Enclosure reasonable effectiveness measures, although those effectiveness measures failed to demonstrate sustained improvement.
prevent equipment from being returned to full service without a review of all corrective
  P.1.d Results  The inspectors sampled input data and observed that Wolf Creek had self-critical internal performance measures because those measurement methods and inputs were
actions by a senior reactor operator. The inspectors concluded that the added problem
found to reflect NRC identified and licensee
evaluation scrutiny was consistent with the identified causes. Although many methods
-identified issues.  The internal metrics for trends in closure of condition reports, corrective action age, and
of finding, evaluating, and fixing problems can work across the power reactor industry,
the maintenance backlog show recent positive improvement.
Wolf Creek chose to make CAP changes while instituting new guidance on the
  The condition report 23032 measures of effectiveness stated that the root cause actions will be effective when the equipment reliability index and performance index reflect sustained improvement.
accountability of the CAP. Based on a sampling review, the inspectors concluded that
The inspectors reviewed the equipment reliability index and found that it is a culmination of several sub
the corrective actions were appropriate to address the identified causes.
indicators
P.1.a Corrective Action Effectiveness Measures
, which was  
Wolf Creek internal metrics consisted of monitoring and trending the condition report
Red until April 2012 when it became
initiation rate overall by the site and department. Identification of the issues by the NRC
Yellow. One important indicator the inspectors
or other organizations, rather than by licensee personnel, negatively impact the metric.
reviewed was the critical equipment failure indicator. The inspectors noted that this indicator
Condition report initiation rate metrics showed a steady increase with most departments
went from
having a high self identification rates in Green with the exception of three in the Red due
White to Red to White over the last year. The inspectors observed that there was not sustained improvement in these internal metrics. The inspectors found a significant challenge in the number
to NRC and external organization identification. The inspectors concluded that the
of open corrective actions in response to NRC violations and findings.  The inspectors reviewed effectiveness followup evaluations for findings and violations in NRC inspection reports, and found these effectiveness follow
licensee had developed reasonable effectiveness measures, and that those
-ups to be sufficiently untimely that they may not provide
effectiveness measures demonstrated an improving trend for the station, but that the red
an independent check prior to recurrence or prevent unnecessary
indicators reflected a continuation of a long standing trend in those areas.
corrective action delay.  With a large backlog and many long term actions, effectiveness follow
P.1.a Results
-ups continue to wait for final corrective action completion
The inspectors observed a low threshold for problems and condition reports. Personnel
because the licensee had no process to perform interim effectiveness reviews when long
interviewed indicated no hesitation to initiate condition reports. The inspectors observed
-term actions were assigned. For example, the inspectors reviewed an open corrective action to install heat tracing for boric acid piping. The modification was complete, but relief valves have not been installed and Wolf Creek was having to rel y on a control room annunciator to have operators respond prior to over
several issues had two or more condition reports for the same problem. Some problems
-pressurization of piping.  No time limit was given to the annunciator response. 
were consolidated to one condition report while others were not. More than one person
The inspectors calculated the operator's time limit to respond by using the heat trace kilowatt rating and the heat capacity of the piping and water. The inspectors found that operators had a reasonable amount of time, but Wolf Creek initiated condition report 54278 to add a time constraint.  Despite this corrective action being over 3 years old and having
or work group may write a condition report for the same problem. Condition report
three effectiveness follow
problem statements for those condition reports were not always reconciled to ensure
-up extensions, corrective action was not complete at the time of the inspection
that all aspects would be corrected. This was consistent with the observations of the
because the relief valves had not been procured.   The inspectors also
biennial problem identification and resolution inspection documented in Inspection
reviewed two issues related to NRC
Report 2012007.
-identified problems with emergency diesel generator testing.  The inspectors found that the issue occurred a second time due to inadequate corrective actions from a previous finding.  The issue
P.1.c Entry into the CAP
was work in progress and thus was considered to be a minor issue within the inspection program. Also, open corrective actions were inappropriately categorized as 'enhancement
                                          - 28 -                            Enclosure
s' to fix the post
 
-maintenance testing deficiency.  Wolf Creek subsequently wrote action 49551
Wolf Creek addressed all P.1 substantive crosscutting issues in two main condition
-02-01 to make the necessary changes.
reports and one condition report from 2008. Condition report 23032 was a root cause
  The inspectors concluded that progress was being made toward implementing the corrective actions for this
evaluation completed for a second time in September 2010. Condition report 23032 was
substantive cross
in response to the problem identification and resolution and human performance
-cutting issue, but that sustained improvement in the quality and timeliness of evaluations had not been demonstrated.
substantive crosscutting issues that led the site to being placed in Column III of the
 
NRCs action matrix. Wolf Creek identified 63 corrective actions that were to correct the
  - 34 - Enclosure  Overall Observations and Conclusion
problem identification and resolution problems. Condition report 34455 also
s  Wolf Creek showed improvement in all three substantive cross
documented a root cause analysis in response to the 2010 end of cycle assessment
-cutting areas by its internal effectiveness measures and by a reduced number
letter from the NRC. Condition report 34455 identified 27 corrective actions. In the past,
of NRC findings with those crosscutting attributes. Wolf Creek has instituted many internal performance measures
Wolf Creek also took action under condition report 2008-8810 for the P.1.c substantive
as corrective actions.
crosscutting issue. The causes for 2008-8810 were nearly identical to the more recent
  Every station has a policy or overarching safety guidance document.  Wolf Creek has made changes to that policy and instituted new ones for a
root causes. The inspectors concluded that the licensee appropriately entered this issue
healthy safety culture. In addition to the station's policy, each department has developed its own
into the CAP.
policy.  Wolf Creek made changes to its accountability of personnel for problem identification and resolution and other aspects of safety culture.  This
P.1.c Causes
includes changes to Wolf Creek's enforcement of these policies. 
Root and apparent causes have been self-critical and they found a lack of management
The inspectors observed that previous efforts to reinforce theses practices and organizational values
involvement and oversight in the corrective action program over the last 3 years. These
have not been successful. The inspectors interviewed selected personnel about the safety culture changes. All staff interviewed
were the same causes identified for White performance indicators that the 95002 team
welcomed changes to fix problems promptly, but their feedback was mixed as to the effectiveness of changes such as procedures and training. Nearly all interviewees expressed concern about their work load and station's ability to correct problems.
examined under condition report 23032. Root cause 34455 has a similar root cause of
    4OA6 Meetings, Including Exit
leadership not aligning station behaviors for timely problem identification and resolution.
Exit Meeting Summary
Root Cause 34455 was written in March 2011 in response to the NRCs 2010
On April 26, 2012, the inspectors presented the results of the radiation safety inspection
Assessment Letter, with the cause evaluation not completed until June 30, 2011. Root
to Mr. M. Sunseri, President and
cause 34455 had a contributing cause of the station having poor training on the design
Chief Executive Officer, and other members of the licensee staff.  The licensee acknowledged the issues presented.  The inspectors asked the licensee whether any materials examined during the inspection should be considered proprietary. No proprietary  
and licensing basis which is inhibiting effective problem evaluation. A contributing cause
was the over-reliance on the work control process to getting problems fixed. Wolf Creek
has repeatedly found that less than timely evaluations have contributed to delays in
corrective actions for substantive cross cutting issues. The inspectors concluded that
the licensee effectively identified the causes for this substantive crosscutting issue.
P.1.c Corrective Actions
The inspectors sampled corrective actions. The previous large change in the corrective
action program was to create the single point of entry for all issues into the CAP. This
eliminated the previous practice of writing a work order for a problem, and only allowed
writing a condition report for each problem. While either method would work, the new
method added working level and management level scrutiny to each condition report.
The licensee recently implemented an important programmatic change involving
changes to the corrective action program software. Although it does not appear to be
directly linked to root cause 23032, a new department was formed which adds more
oversight to operability determinations and work control, which is responsive the root
causes. Changes were made to track and evaluate degraded or non-conforming
conditions with a new department named operations work control. The inspectors
observed that the more recent immediate operability evaluations more closely tie the
equipment requirements to the observed problems to confirm or refute operability or
functionality (P.1.c). Also, the new changes track each degraded condition and
equipment cannot be returned to full service without review of all corrective actions by a
senior reactor operator (P.1.d). The inspectors found the added problem evaluation
                                        - 29 -                            Enclosure
 
scrutiny is consistent with the causes. Although many methods of finding, evaluating,
and fixing problems can work across the power reactor industry, Wolf Creek chose to
make CAP changes while instituting new guidance on the accountability of the CAP.
Most other corrective actions centered on recurring training for cause evaluators and
procedure changes to corrective action procedures, both directed at increasing the
quality of condition report causal evaluations.
P.1.c Corrective Action Effectiveness Measures.
The licensee developed evaluation quality internal performance indications, including the
results from corrective action review board and other challenge boards. The results of
these metrics were trending in a positive direction. These quality metrics and oversight
boards have undergone many changes in the last two years. The inspectors observed
that the trends reflect the refueling and forced outages, which typically cause an
increase in the number of evaluations needed. The operability evaluation metric up to
May showed a declining trend in quality over the last 6 months, though inspectors noted
that Wolf Creek did not find any evaluations that failed to demonstrate operability. Root
and apparent cause evaluation completion timeliness goals showed an improving trend
since October 2011, but are still Red and do not show average completion times that are
close to procedural limits. The inspectors concluded that the licensee had developed
reasonable effectiveness measures, although those effectiveness measures failed to
demonstrate sustained improvement.
P.1.c Results
Creating a single point of entry into the CAP was a significant change. The changes to
improve tracking of degraded or non-conforming conditions added some priority to fixing
problems, but giving priority to these types of items is still not a formal process
requirement. Corrective actions are still largely prioritized in the work control process.
Most corrective actions have focused on improving condition report evaluation
timeliness, providing evaluation methodology training (why tree, hazard-barrier-target,
etc.), and improving coding and trending of causes.
The inspectors interviewed department corrective action coordinators and found that
they had an active role in trending recurring problems in each department. The
inspectors saw this as a positive change but not directly related to evaluation quality.
Training on the plant design bases was positive and provided information on the overall
regulatory framework, but did not include specific requirements for the trainees systems
or engineering discipline. The inspectors saw improvement in the rejection of the root
cause by the corrective action review board for the January 13, 2012, loss of offsite
power, although not all rejections were captured by the stations metric.
The inspectors reviewed Wolf Creeks comprehensive event safety-significance
evaluation which examined all the problems revealed during the January 13, 2012, loss
of offsite power. Problem evaluation was stated as a contributing cause in that
self-assessment. Corrective actions were deferred to an apparent cause evaluation
stemming from a quality assurance audit that found the corrective action program
marginally effective. Corrective actions to that quality assurance assessment continued
the trend of changes to cause method training and CAP procedure changes. With
                                        - 30 -                              Enclosure
 
design basis training being a self-identified weakness, inspectors observed that the
number and high-level content of those training courses will challenge the adequacy of
equipment specific problems, such as the leak seal repair in this report. The inspectors
concluded that progress was being made toward implementing the corrective actions for
this substantive cross-cutting issue, but that sustained improvement in the quality and
timeliness of evaluations had not been demonstrated.
P.1.d Entry into the CAP
Wolf Creek addressed all P.1 substantive crosscutting issues in two main condition
reports. Condition report 23032 was a root cause evaluation completed for a second
time in September 2010. Condition report 23032 was in response to the problem
identification and resolution and human performance substantive crosscutting issues
that led the site to Column III of the NRCs action matrix. Wolf Creek identified 63
corrective actions that were to correct the problem identification and resolution problems.
Condition report 34455 was also a root cause in response to the 2010 end of cycle
assessment letter from the NRC. Condition report 34455 identified 27 corrective actions.
The inspectors concluded that the licensee appropriately entered this issue into the
CAP.
P.1.d Causes
Root and apparent cause evaluations for this substantive cross-cutting issue were self-
critical, and they documented a lack of management involvement and oversight in the
corrective action program over the last 3 years. These are the same causes the 95002
team examined under condition report 23032. Root cause 34455 had a similar root
cause of leadership not aligning station behaviors for timely problem identification and
resolution. Root cause 34455 had a contributing cause of the station having inadequate
training on the design and licensing basis which was inhibiting effective problem
evaluation. These causes are the same as those for the P.1.a and P.1.c substantive
cross-cutting issues. The previous large change in the corrective action program was to
create the single point of entry for all issues into the CAP. This eliminated the previous
practice of writing a work order for a problem, and only allowed writing a condition report
for each problem. While either method would work, the new method added working
level and management level scrutiny to each condition report. The licensee recently
implemented an important programmatic change involving changes to the corrective
action program software. Although it does not appear to be directly linked to root cause
23032, a new department was formed which adds more oversight to operability
determinations and work control, which is responsive the root causes Changes were
made to track and evaluate degraded or non-conforming conditions with a new
department named operations work control. The inspectors observed that the more
recent immediate operability evaluations were more closely tied the equipment
requirements to the observed problems in order to be able to confirm or refute operability
or functionality. Also, the new changes track each degraded condition, and required that
equipment cannot be returned to full qualification without review of all corrective actions
by a senior reactor operator. The inspectors concluded that the increased problem
evaluation scrutiny was consistent with the causes. Although many methods of finding,
evaluating, and fixing problems can work across the power reactor industry, Wolf Creek
chose to make CAP changes while instituting new guidance on the accountability of the
                                          - 31 -                          Enclosure
 
CAP. The inspectors concluded that the licensee effectively identified the causes for this
substantive crosscutting issue.
P.1.d Corrective Actions
The inspectors reviewed selected corrective actions that were most responsive to the
root causes. Condition report 23032, action 2-9, instituted on August 31, 2011, required
the corrective actions review board review each issue coded as being a corrective action
to prevent recurrence within 30 days of its closure. Separate from the root causes, the
inspectors found other condition reports responding to NRC violations on annunciator
power supplies, emergency diesel loading, operability evaluations, and maintenance rule
stating that there was a need for continuing engineering training on standards for each of
those issues. The inspectors reviewed training lesson plans for change package
continuing training [modifications], Regulatory, Current Licensing Basis, And Design
Basis, and operability evaluation training for engineers and licensed operators. The
inspectors observed that the training was conducted every 60 days. Wolf Creek has
instituted corrective action backlog measurement indicators as a corrective action. The
inspectors noted that the act of trending is not a corrective action. Those backlogs
remain high, but have made some progress since the forced outage earlier this year.
Engineering also had a significant backlog of over 5500 work orders in May 2012. The
corrective action backlog initiative plan required regular meetings for departments to
drive a reduction in their backlog, but no other specific actions were developed, such as
addressing actions by priorities. The inspectors also noted that there were a significant
number of open actions to correct NRC violations, especially for scoping of maintenance
rule functions. Based on a sampling review, the inspectors concluded that the
corrective actions to address this substantive cross-cutting aspect were partially
appropriate to address the identified causes, but specific actions to ensure that CAP
corrective actions were timely and effective were lacking.
P.1.d Corrective Action Effectiveness Measures
Wolf Creeks effectiveness review for root cause condition report 23032 concluded that
there was not sustained improvement in ensuring that corrective actions were timely and
effective due to not meeting internal station metrics set for maintenance backlogs,
repetitive maintenance rule functional failures, and two other failed effectiveness follow-
ups. The interim effectiveness follow-up for root cause condition report 34455 was met
with the exception of one internal performance indicator for too great a ratio of NRC
identified to licensee identified findings. The inspectors observed that the identification
credit is an NRC function and affects the indicator, which may not be insightful. The
conclusion of condition report 34455 interim effectiveness review stated that additional
time was needed to increase the internal self-identification metrics and that more time
was needed. This effectiveness review also gave credit for future expected
improvement in the equipment performance index, a licensee metric, and which was
Yellow at the time of the inspection. The final effectiveness follow-up was scheduled to
be completed by December 20, 2012. The non-cited violation closure effectiveness
performance indicator was Red in January, February, and March 2012. Wolf Creek has
written two condition reports on the non-cited violation effectiveness performance
indicator and the need to return it to Green and are due to have formulated corrective
actions by August 9, 2012. The inspectors concluded that the licensee had developed
                                          - 32 -                          Enclosure
 
reasonable effectiveness measures, although those effectiveness measures failed to
demonstrate sustained improvement.
P.1.d Results
The inspectors sampled input data and observed that Wolf Creek had self-critical
internal performance measures because those measurement methods and inputs were
found to reflect NRC identified and licensee-identified issues. The internal metrics for
trends in closure of condition reports, corrective action age, and the maintenance
backlog show recent positive improvement. The condition report 23032 measures of
effectiveness stated that the root cause actions will be effective when the equipment
reliability index and performance index reflect sustained improvement. The inspectors
reviewed the equipment reliability index and found that it is a culmination of several sub
indicators, which was Red until April 2012 when it became Yellow. One important
indicator the inspectors reviewed was the critical equipment failure indicator. The
inspectors noted that this indicator went from White to Red to White over the last year.
The inspectors observed that there was not sustained improvement in these internal
metrics.
The inspectors found a significant challenge in the number of open corrective actions in
response to NRC violations and findings. The inspectors reviewed effectiveness
followup evaluations for findings and violations in NRC inspection reports, and found
these effectiveness follow-ups to be sufficiently untimely that they may not provide an
independent check prior to recurrence or prevent unnecessary corrective action delay.
With a large backlog and many long term actions, effectiveness follow-ups continue to
wait for final corrective action completion because the licensee had no process to
perform interim effectiveness reviews when long-term actions were assigned. For
example, the inspectors reviewed an open corrective action to install heat tracing for
boric acid piping. The modification was complete, but relief valves have not been
installed and Wolf Creek was having to rely on a control room annunciator to have
operators respond prior to over-pressurization of piping. No time limit was given to the
annunciator response. The inspectors calculated the operators time limit to respond by
using the heat trace kilowatt rating and the heat capacity of the piping and water. The
inspectors found that operators had a reasonable amount of time, but Wolf Creek
initiated condition report 54278 to add a time constraint. Despite this corrective action
being over 3 years old and having three effectiveness follow-up extensions, corrective
action was not complete at the time of the inspection because the relief valves had not
been procured.
The inspectors also reviewed two issues related to NRC-identified problems with
emergency diesel generator testing. The inspectors found that the issue occurred a
second time due to inadequate corrective actions from a previous finding. The issue
was work in progress and thus was considered to be a minor issue within the inspection
program. Also, open corrective actions were inappropriately categorized as
enhancements to fix the post-maintenance testing deficiency. Wolf Creek subsequently
wrote action 49551-02-01 to make the necessary changes. The inspectors concluded
that progress was being made toward implementing the corrective actions for this
substantive cross-cutting issue, but that sustained improvement in the quality and
timeliness of evaluations had not been demonstrated.
                                        - 33 -                          Enclosure
 
        Overall Observations and Conclusions
        Wolf Creek showed improvement in all three substantive cross-cutting areas by its
        internal effectiveness measures and by a reduced number of NRC findings with those
        crosscutting attributes. Wolf Creek has instituted many internal performance measures
        as corrective actions. Every station has a policy or overarching safety guidance
        document. Wolf Creek has made changes to that policy and instituted new ones for a
        healthy safety culture. In addition to the stations policy, each department has
        developed its own policy. Wolf Creek made changes to its accountability of personnel
        for problem identification and resolution and other aspects of safety culture. This
        includes changes to Wolf Creeks enforcement of these policies. The inspectors
        observed that previous efforts to reinforce theses practices and organizational values
        have not been successful. The inspectors interviewed selected personnel about the
        safety culture changes. All staff interviewed welcomed changes to fix problems
        promptly, but their feedback was mixed as to the effectiveness of changes such as
        procedures and training. Nearly all interviewees expressed concern about their work
        load and stations ability to correct problems.
4OA6 Meetings, Including Exit
Exit Meeting Summary
On April 26, 2012, the inspectors presented the results of the radiation safety inspection to
Mr. M. Sunseri, President and Chief Executive Officer, and other members of the licensee staff.
The licensee acknowledged the issues presented. The inspectors asked the licensee whether
any materials examined during the inspection should be considered proprietary. No proprietary
information was identified.
information was identified.
 
On July 18, 2012, the inspectors presented the inspection results to Mr. Richard Clemens, Vice
On July 18, 2012, the inspectors presented the inspection results to Mr. Richard Clemens, Vice President of Strategic Projects, and other members of the licensee staff. The licensee acknowledged the issues presented. The inspector asked the licensee whether any materials  
President of Strategic Projects, and other members of the licensee staff. The licensee
examined during the inspection should be considered proprietary. All proprietary information was returned or destroyed
acknowledged the issues presented. The inspector asked the licensee whether any materials
4OA7 Licensee-Identified Violations
examined during the inspection should be considered proprietary. All proprietary information
The following violation of very low safety significance (Green) was identified by the licensee and is a violation of NRC requirements which meet s the criteria of the NRC Enforcement Policy for being dispositioned as a  
was returned or destroyed.
n on-cited violation. .1 On January 31, 2012, Wolf Creek identified that  
4OA7 Licensee-Identified Violations
inservice inspection for the second  
The following violation of very low safety significance (Green) was identified by the licensee and
10-year period were missed for two valves. Valves BB8379A and BB8379B are chemical and volume control system alternate charging check valves to reactor coolant system loop four. Both are ASME Code Class
is a violation of NRC requirements which meets the criteria of the NRC Enforcement Policy for
1 valves. In 1987, valve BB8379B had a leak at the body
being dispositioned as a non-cited violation.
-to-bonnet joint and its studs were re
.1       On January 31, 2012, Wolf Creek identified that inservice inspection for the second
-torqued. The valve continued to leak a small amount. Subsequently, valves BB8379A and BB8379B each had a seal cap, or leakage control device, installed on December 9, and 28, 1987, respectively.  
        10-year period were missed for two valves. Valves BB8379A and BB8379B are
  - 35 - Enclosure Title 10 CFR 50.55a(g)(4) requires licensees to follow the pressure test requirements of the ASME Code Section XI. ASME Code, Section XI, IWA
        chemical and volume control system alternate charging check valves to reactor coolant
-5240 , requires visual examinations as part of system pressure tests. ASME Code Section XI, IWA
        system loop four. Both are ASME Code Class 1 valves. In 1987, valve BB8379B had a
-5242 , 1998 Edition through 2000 addenda, requires pressure retaining bolted connections for  
        leak at the body-to-bonnet joint and its studs were re-torqued. The valve continued to
VT-2 visual examinations in borated water systems. Contrary to the above, from September 3, 1995
        leak a small amount. Subsequently, valves BB8379A and BB8379B each had a seal
, to the present, Wolf Creek did not perform a visual inspection of the valve body
        cap, or leakage control device, installed on December 9, and 28, 1987, respectively.
-to-bonnet studs. This finding was more than minor because it impacted the Initiating Events Cornerstone and its attribute of equipment performance. Specifically, it affected the objective to limit the likelihood of those events that upset plant stability and  
                                                  - 34 -                           Enclosure
challenge critical safety functions during shutdown as well as power operations. Using Inspection Manual Chapter 0609
 
, Appendix A  
Title 10 CFR 50.55a(g)(4) requires licensees to follow the pressure test requirements of
,"The Significance Determination Process (SDP) for Findings At
the ASME Code Section XI. ASME Code, Section XI, IWA-5240, requires visual
-Power," this finding was determined to be of very low safety significance because an evaluation was able to demonstrate structural integrity.
examinations as part of system pressure tests. ASME Code Section XI, IWA-5242,
Specifically, stud stress was not sufficiently close to the yield stress to cause a loss of  
1998 Edition through 2000 addenda, requires pressure retaining bolted connections for
integrity. Therefore, the finding does not contribute to both the likelihood of a reactor trip and the likelihood that mitigation equipment will not be available.
VT-2 visual examinations in borated water systems. Contrary to the above, from
  The licensee has entered this issue into their corrective action program as condition reports 48493 and 48494. Wolf Creek plan
September 3, 1995, to the present, Wolf Creek did not perform a visual inspection of the
ned to remove the seal caps and perform the inspection in the next refueling outage.
valve body-to-bonnet studs. This finding was more than minor because it impacted the
 
Initiating Events Cornerstone and its attribute of equipment performance. Specifically, it
  A-1 Attachment
affected the objective to limit the likelihood of those events that upset plant stability and
SUPPLEMENTAL INFORMATION
challenge critical safety functions during shutdown as well as power operations. Using
  KEY POINTS OF CONTACT  
Inspection Manual Chapter 0609, Appendix A ,The Significance Determination Process
  Licensee Personnel     T. Baban, Manager, Systems Engineering  
(SDP) for Findings At-Power, this finding was determined to be of very low safety
P. Bedgood, Manager, Radiation Protection  
significance because an evaluation was able to demonstrate structural integrity.
J. Broschak, Vice President, Engineering  
Specifically, stud stress was not sufficiently close to the yield stress to cause a loss of
S. Carpenter, Technician, Instruments and Controls
integrity. Therefore, the finding does not contribute to both the likelihood of a reactor trip
R. Clemons, Vice President, Strategic Projects  
and the likelihood that mitigation equipment will not be available. The licensee has
D. Dees, Superintendant, Operations
entered this issue into their corrective action program as condition reports 48493 and
T. East, Superintendent, Emergency Planning  
48494. Wolf Creek planned to remove the seal caps and perform the inspection in the
R. Evenson, Requalification Program Supervisor  
next refueling outage.
R. Flannigan, Manager, Nuclear Engineering  
                                          - 35 -                            Enclosure
K. Fredrickson, Engineer, Licensing
 
D. Gibson, Technician, Radiation Protection
                                  SUPPLEMENTAL INFORMATION
R. Hammond, Supervisor, Regulatory Support
                                    KEY POINTS OF CONTACT
J. Harris, System Engineer  
Licensee Personnel
S. Henry, Operations Manager  
T. Baban, Manager, Systems Engineering
R. Hobby, Licensing Engineer  
P. Bedgood, Manager, Radiation Protection
S. Hossain, Engineer, System Engineering
J. Broschak, Vice President, Engineering
T. Jensen, Manager, Chemistry  
S. Carpenter, Technician, Instruments and Controls
T. Just, Senior Technician, Chemistry  
R. Clemons, Vice President, Strategic Projects
J. Keim, Support Engineering Supervisor  
D. Dees, Superintendant, Operations
S. Koenig, Manager, Corrective Actions  
T. East, Superintendent, Emergency Planning
M. McMullen, Technician, Engineering  
R. Evenson, Requalification Program Supervisor
R. Flannigan, Manager, Nuclear Engineering
K. Fredrickson, Engineer, Licensing
D. Gibson, Technician, Radiation Protection
R. Hammond, Supervisor, Regulatory Support
J. Harris, System Engineer
S. Henry, Operations Manager
R. Hobby, Licensing Engineer
S. Hossain, Engineer, System Engineering
T. Jensen, Manager, Chemistry
T. Just, Senior Technician, Chemistry
J. Keim, Support Engineering Supervisor
S. Koenig, Manager, Corrective Actions
M. McMullen, Technician, Engineering
C. Medenciy, Supervisor, Radiation Protection
C. Medenciy, Supervisor, Radiation Protection
W. Muilenburg, Licensing Engineer  
W. Muilenburg, Licensing Engineer
M. McMullen, Design Engineer, Engineering
M. McMullen, Design Engineer, Engineering
K. Miller, Technician Level III, Instruments and Controls
K. Miller, Technician Level III, Instruments and Controls
R. Murray, Simulator Supervisor  
R. Murray, Simulator Supervisor
E. Ray, Manager, Training  
E. Ray, Manager, Training
L. Ratzlaff, Manager, Maintenance  
L. Ratzlaff, Manager, Maintenance
T. Rice, Manager, Environmental Management
T. Rice, Manager, Environmental Management
L. Rockers, Licensing Engineer  
L. Rockers, Licensing Engineer
R. Ruman, Manager, Quality  
R. Ruman, Manager, Quality
G. Sen, Regulatory Affairs Manager
G. Sen, Regulatory Affairs Manager  
D. Scrogum, Systems Engineer, Engineering
D. Scrogum, Systems Engineer, Engineering
R. Smith, Plant Manager
L. Solorio, Senior Engineer
R. Smith, Plant Manager  
M. Sunseri, President and Chief Executive Officer
L. Solorio, Senior Engineer  
J. Truelove, Supervisor, Chemistry
M. Sunseri, President and Chief Executive Officer  
J. Weeks, System Engineer
J. Truelove, Supervisor, Chemistry J. Weeks, System Engineer  
M. Westman, Assistant to Site Vice President
M. Westman, Assistant to Site Vice President  
                    LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
  LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED  
                                                A-1            Attachment
 
 
  A-2 Opened and Closed
Opened and Closed
05000482/2012003
05000482/2012003-01 NCV         Unacceptable Leakage Through Safety Related Watertight Door
-0 1 NCV Unacceptable Leakage  
                                During Loss of Offsite Power (Section 1R06)
Through Safety Related Watertight Door  
05000482/2012003-02 NCV         Incorrect Leak Seal Injection Port Installation.
During Loss of Offsite Power (Section 1R06) 05000482/2012003
                                (Section 1R18)
-0 2 NCV Incorrect Leak Seal Injection Port Installation."
Closed
  (Section 1R18) Closed 05000482/2012-03-00 LER Train B ECCS Inoperable Due to Damaged Watertight Containment Spray Pump Door Seal (Section 4OA3)   LIST OF DOCUMENTS REVIEWED
05000482/2012-03-00   LER       Train B ECCS Inoperable Due to Damaged Watertight
  Section 1R
                                Containment Spray Pump Door Seal (Section 4OA3)
01: Adverse Weather Protection
                          LIST OF DOCUMENTS REVIEWED
PROCEDURES
Section 1R01: Adverse Weather Protection
NUMBER TITLE REVISION OFN SG-003 Natural Events
PROCEDURES
22 AI 14-006 Severe Weather
    NUMBER                                   TITLE                               REVISION
1 2 OFN AF-025 Unit Limitations
OFN SG-003       Natural Events                                                       22
36 DRAWINGS   A-1320 Fuel Building Floor Plan  
AI 14-006         Severe Weather                                                       12
2047'-6" and Roof
OFN AF-025       Unit Limitations                                                     36
0 MISCELLANEOUS
DRAWINGS
  OpESS 2012/01
A-1320           Fuel Building Floor Plan 2047-6 and Roof                           0
Operating Experience Smart Sample "
MISCELLANEOUS
High Wind Generated Missile hazards
OpESS 2012/01     Operating Experience Smart Sample High Wind Generated               0
" 0  CONDITION REPORTS
                  Missile hazards
51552 51562 46940   Section 1R
CONDITION REPORTS
04: Equipment Alignment
51552           51562               46940
PROCEDURES
Section 1R04: Equipment Alignment
NUMBER TITLE REVISION SYS GK-200 Inoperable Class IE A/C Unit
PROCEDURES
24 SYS EM-120 BIT Depressurization
    NUMBER                                   TITLE                               REVISION
2
SYS GK-200     Inoperable Class IE A/C Unit                                         24
  A-DRAWINGS NUMBER TITLE REVISION M-12EM01 Piping & Instrumentation Diagram High Pressure Coolant Injection System
SYS EM-120     BIT Depressurization                                                 2
38 M-12EM02 Piping & Instrumentation Diagram High Pressure Coolant Injection System
                                            A-2
19  CONDITION REPORTS
 
  00053393 00053472 00053452 00053549 00053625 00053671 00053672 00053685 00053696 00053703 00053709 00053710 00053791 00053785 00053793 00053796 00053798 00048882   Section 1R
DRAWINGS
05: Fire Protection
  NUMBER                                     TITLE                           REVISION
PROCEDURES
M-12EM01         Piping & Instrumentation Diagram High Pressure Coolant           38
NUMBER TITLE REVISION AP 10-106 Fire Preplans
                Injection System
12 AP 10-104 Breach Authorization
M-12EM02         Piping & Instrumentation Diagram High Pressure Coolant           19
26  DRAWINGS NUMBER TITLE REVISION E-1F9905 Fire Hazard Analysis, Fire Area A
                Injection System
-13 (Reference A
CONDITION REPORTS
-1803) 4 E-1F9905 Fire Hazard Analysis, Fire Area A
00053393         00053472           00053452           00053549         00053625
-14 (Reference A
00053671         00053672           00053685           00053696         00053703
-1804) 4 E-1F9905 Fire Hazard Analysis, Fire Area A
00053709         00053710           00053791           00053785         00053793
-15 (Reference A
00053796         00053798           00048882
-1804) 4 M-663-00017A Fire Protection Evaluations for Unique or Unbounded Fire Barrier Configurations
Section 1R05: Fire Protection
Section 1R
PROCEDURES
06: Flood Protection Measures
  NUMBER                                     TITLE                         REVISION
PROCEDURE NUMBER TITLE REVISION MPM XX-002 Water Tight Door Preve
  AP 10-106                               Fire Preplans                           12
ntive Maintenance Activity
  AP 10-104                         Breach Authorization                         26
CONDITION REPORTS
DRAWINGS
 
  NUMBER                                     TITLE                         REVISION
  A-4 51570 51622 52975 52794   Section 1R11: Licensed Operator Requalification Program
E-1F9905         Fire Hazard Analysis, Fire Area A-13 (Reference A-1803)       4
  MISCELLANEOUS
E-1F9905         Fire Hazard Analysis, Fire Area A-14 (Reference A-1804)       4
NUMBER TITLE REVISION LR4607005 Requal Simulator Exam Scenario  
E-1F9905         Fire Hazard Analysis, Fire Area A-15 (Reference A-1804)       4
2 AP 21-001 Conduct of Operations
M-663-00017A     Fire Protection Evaluations for Unique or Unbounded           3
57  Section 1R12: Maintenance Effectiveness
                  Fire Barrier Configurations
  PROCEDURES
Section 1R06: Flood Protection Measures
NUMBER TITLE REVISION WCOP-24 Operations EMG/OFN Setpoints
PROCEDURE
8 STN AE-007 Startup Main Feedwater Pump Operational Test
  NUMBER                                     TITLE                         REVISION
2 and 3 AP 16E-002 Post Maintenance Testing Development
MPM XX-002       Water Tight Door Preventive Maintenance Activity                   4
10 and 11 MDI 06-01 Guidelines for Work Order Peer Review
CONDITION REPORTS
6 EDI 23M-050 Engineering Desktop Instruction Monitoring Performance to Criteria and Goals
                                              A-3
8 STS ML-001 Monthly Surveillance Log
 
45 SB-01 Reactor Protection systems
51570           51622             52975             52794
  CONDITION REPORTS
Section 1R11: Licensed Operator Requalification Program
  51655 51706 41997 53417 35413 35426 35532 35533 35535 35537 35539 35540 35541 35542 35544 35545 35546 35547 35548 35549 35550 35551 35552 35553 35554 35555 35558 35560 35614 35615 35617 35619 35620 35621 35622 35623 35624 35625 35626 35627 35628 35629 35882 36012 35013 36014 36038 36039 36040 36041 36042 36043 36044 36045 36057
MISCELLANEOUS
  A-5 36058 36060 36061 36062 36064 36065 36078 36079 36080 36081 36082 3608336084
  NUMBER                                 TITLE                             REVISION
36117 36118 36119 36134 36135 38108 40687 40753 46341 48955 49672 49738   WORK ORDER 11-346146-003     PERFORMANCE IMPROVEMENT REQUEST
LR4607005       Requal Simulator Exam Scenario                                   2
36518 36777 37048 37107 37439 37482 37615 38003 38023 38106 38162 38108 38369 38487 38488 38873 39349 39350 39351 39365 43639 49672 54110 54163 54164 45414     CALCULATIONS
AP 21-001       Conduct of Operations                                           57
NUMBER TITLE REVISION AN-11-007 Startup Feedwater Pump (PAE02) Flow Rate Required to Remove Decay Heat Following Reactor Shutdown
Section 1R12: Maintenance Effectiveness
DRAWINGS NUMBER TITLE REVISION M-12AE01 Piping & Instrumentation Diagram Feedwater System
PROCEDURES
38  Section 1R13: Maintenance Risk Assessment and Emergent Work Controls
  NUMBER                                   TITLE                             REVISION
PROCEDURES
WCOP-24         Operations EMG/OFN Setpoints                                       8
NUMBER TITLE REVISION NK-022 Load Test 2 STS-MT-020 125 Volt DC Battery Inspection/Charger Operational Test
STN AE-007       Startup Main Feedwater Pump Operational Test                   2 and 3
25B  CONDITION REPORTS
AP 16E-002       Post Maintenance Testing Development                         10 and 11
 
MDI 06-01       Guidelines for Work Order Peer Review                             6
  A-6 51421 51565     WORK ORDERS
EDI 23M-050     Engineering Desktop Instruction Monitoring Performance to         8
  06-281938-000 04-259540-000 04-259542-000 12-353322-000 12-353322-001 DRAWINGS NUMBER TITLE REVISION E-051-00058 Three phase SCR Controller Battery Charger Schematic
                Criteria and Goals
WO7 WIP-M-761-00075-W08-A-1 SNUPPS Process Control Block Diagram+
STS ML-001       Monthly Surveillance Log                                         45
00  MISCELLANEOUS
SB-01           Reactor Protection systems
NUMBER TITLE DATE N/A On-Line Nuclear safety and Generation Risk Assessment
CONDITION REPORTS
May 30, 2012
51655           51706               41997             53417             35413
  Section 1R15: Operability Evaluations
35426           35532               35533             35535             35537
DRAWINGS NUMBER TITLE REVISION M-724-00276 Swing Check Valve
35539           35540               35541             35542             35544
W04 OE BB12-004 BB8397A/B CVCS Alternate Charging to Loop 4 Check Valve 1 MGM MOOP-08 Torquing Guidelines for Bolted Connections
35545           35546               35547             35548             35549
13 RR-87-060 ASME Section XI Repair/Replacement Plan
35550           35551               35552             35553             35554
0 RR-87-060 ASME Section XI Repair/Replacement Plan
35555           35558               35560             35614             35615
PROCEDURES
35617           35619               35620             35621             35622
NUMBER TITLE REVISION EPP 06-002 Technical Support Center Operations
35623           35624               35625             35626             35627
30A EPP 06-013 Exposure Control and Personnel Protection
35628           35629               35882             36012             35013
6 EMG E-0 Reactor Trip or Safety Injection
36014           36038               36039             36040             36041
27  CALCULATION
36042           36043               36044             36045             36057
S NUMBER TITLE REVISION AN 99-020 Control Room Habitability of a Postulated LOCA, based on a Control Room Unfiltered Inleakage of 20.0 cfm
                                          A-4
 
  A-7 CALCULATION
36058           36060             36061             36062             36064
S NUMBER TITLE REVISION GK-M-001 Safety Related Control Room Building HVAC Capabilities During Accident Conditions (SGK04A/B and SGK05A/B)
36065           36078             36079             36080             36081
2 GK-E-001 Electrical Equipment Heat Loads in ESF SWGR, DC SWBD, & Battery Rooms  
36082           3608336084         36117             36118             36119
MISCELLANEOUS DOCUMENTS
36134           36135             38108             40687             40753
NUMBER TITLE REVISION / DATE ITLS Report 24045
46341           48955             49672             49738
Liquid Penetrant Inspection of Submitted Machined Parts August 7, 1978
WORK ORDER
  Jessop Steel Company  
11-346146-003
- Ultrasonic Inspection Report
PERFORMANCE IMPROVEMENT REQUESTS
June 28, 1978
36518           36777             37048             37107             37439
  Operability Evaluation OE BB
37482           37615             38003             38023             38106
-12-004 00 Case N-616 Cases of ASME Boiler and Pressure Vessel Code
38162           38108             38369             38487             38488
May 7, 1999
38873           39349             39350             39351             39365
SAP-12-58 Westinghouse LTR
43639           49672             54110             54163             54164
-SEE-III-12-81 April 14, 2012
45414
128136 Westinghouse Drawing Revision  
CALCULATIONS
- Material Changes
    NUMBER                                 TITLE                             REVISION
  September 28, 1993 CA2412 1 st & 2 nd Off Check Valve PMs
AN-11-007       Startup Feedwater Pump (PAE02) Flow Rate Required to           0
December 26, 2008 OE BB12-004 BB8397A/B CVCS Alternate Charging to Loop 4 Check Valve 00 CA4790 Write PMC Work Request
                Remove Decay Heat Following Reactor Shutdown
December 26, 2008 CA4791 Revise AP 23F
DRAWINGS
-001 December 26, 2008 CA4792 Update BID
    NUMBER                                 TITLE                             REVISION
-CV-1 December 26, 2008 M-622.1 (Q) Design Specifcation for Packaged Air Conditioning Units
M-12AE01       Piping & Instrumentation Diagram Feedwater System               38
WORK REQUESTS
Section 1R13: Maintenance Risk Assessment and Emergent Work Controls
  03611-87 00122-87     CONDITION REPORTS
PROCEDURES
  00048493 00048494 00051530 003419 0052822  
    NUMBER                                 TITLE                             REVISION
  A-8 WORK ORERS 07-295490-000 08-309436-000 10-324925-000 10-327516-000 10-327516-001 10-324925-000 10-331280-000 10-327516-000 11-339107-001 11-339107-002 11-339107-000 12-351057-000 00-223094-011   Section 1R18: Plant Modifications
NK-022         Load Test                                                       2
NUMBER TITLE REVISION / DATE BMV0037 Furmanite Adapter Installation Evaluation
STS-MT-020     125 Volt DC Battery Inspection/Charger Operational Test       25B
00 MPM LR-001 Leak Sealant Injection
CONDITION REPORTS
7 WCN-00-001 Reedy Engineering, Inc. No 00
                                          A-5
-216961-000 0 ECW-119 Furmanite The Solutions Group
 
DRAWINGS NUMBER TITLE REVISION / DATE M-240-00072 Valve Assembly  
51421           51565
- 2 IN Diaphragm Y Type, Globe 1522 LB.C.S 1974 ASME Code, Article NC
WORK ORDERS
-3000   1986 ASME Code, NC
06-281938-000   04-259540-000       04-259542-000     12-353322-000   12-353322-001
-3229   1983 ASME Code, NC3232.2
DRAWINGS
  Fig NC3329(g)-1 1986 Edition ASME Code
    NUMBER                                 TITLE                           REVISION
  MPM LR-001 Leak Sealant Injection
E-051-00058     Three phase SCR Controller Battery Charger Schematic           WO7
7 Change Package  
WIP-M-761-     SNUPPS Process Control Block Diagram+                            00
013482 Furnmanite Adapter Fitting and BMV0037 Furmanite Repair
00075-W08-A-1
00 ECW-119 Pressure Seal Calculation Sheet
MISCELLANEOUS
CONDITION REPORT
    NUMBER                                 TITLE                             DATE
  52992     WORK ORDER
N/A             On-Line Nuclear safety and Generation Risk Assessment       May 30, 2012
10-333183-002 10-333183-009 11-346576-002 11-346576-003 11-346576-006 11-346576-009 11-346576-010 11-346576-015 11-346576-017  
Section 1R15: Operability Evaluations
  A-9 Section 1R19: Postmaintenance Testing
DRAWINGS
PROCEDURES
    NUMBER                                   TITLE                         REVISION
NUMBER TITLE REVISION MPE GK-003 Control Room and Class 1E A/C Units Preventive Maintenance Activity
M-724-00276       Swing Check Valve                                           W04
3A MPE GK-004 GK Unit Preparation for Work
OE BB12-004       BB8397A/B CVCS Alternate Charging to Loop 4 Check             1
4 STS IC-500G Channel Calibration DT/TAVG Instrumentation Loop 4
                  Valve
22A STS IC-204A Channel Operational Test of TAVG, dT and Pressurizer Pressure Protection Set Four
MGM MOOP-08       Torquing Guidelines for Bolted Connections                   13
17B INC C-0026 7300 Lead/Lag Card (NLL0G01 Artwork Revisions 12)
RR-87-060         ASME Section XI Repair/Replacement Plan                       0
2A INC C-0016 7300 Summing AMP Card (NSA1 and NSA2)
RR-87-060         ASME Section XI Repair/Replacement Plan                       1
10A STS IC-502B Channel Calibration of 7300 Process Pressurizer Pressure Instrumentation
PROCEDURES
16 STS IC-444 Channel Calibration NIS Power Range N
    NUMBER                                 TITLE                           REVISION
-44 11B WORK ORDERS 12-354805-003 11-348929-000 11-348929-002 11-348929-003 11-348929-004 11-348929-005 12-355385-001 12-355293-001 12-355293-004 12-355293-005 DRAWINGS NUMBER TITLE REVISION E-13GK13A Schematic Diagram Class IE Electri
EPP 06-002     Technical Support Center Operations                             30A
cal Equipment A/C Unit
EPP 06-013     Exposure Control and Personnel Protection                       6
6 QCP-20-514 Eddy Current Examination Technique Sheet
EMG E-0         Reactor Trip or Safety Injection                                 27
5C  Eddy Current Calibration Summaries
CALCULATIONS
  WIP-M-761-02102-004-A-1 Interconnecting wiring diagram cabinet
    NUMBER                                 TITLE                           REVISION
04 SNUPPS Nuclear Power Plant Controls
AN 99-020       Control Room Habitability of a Postulated LOCA, based on a       2
00 WIP-M-761-02088-W08-A-1 Interconnecting wiring diagram cabinet 04 SNUPPS Nuclear Power Plant Controls
                Control Room Unfiltered Inleakage of 20.0 cfm
00 M-761-02084 Interconnecting wiring diagram cabinet 04 SNUPPS Nuclear Power Plant Controls
                                            A-6
W20 
 
  A-10 Section 1R22: Surveillance Testing
CALCULATIONS
PROCEDURES
  NUMBER                                     TITLE                             REVISION
NUMBER TITLE REVISION ABHV0011 Solenoid Block Replacement
GK-M-001         Safety Related Control Room Building HVAC Capabilities               2
  STS AB-205 Main Steam System Inservice Valve Test
                  During Accident Conditions (SGK04A/B and SGK05A/B)
29 6101-00007 CS Innovations LLC 2008 Confidential and Proprietary
GK-E-001         Electrical Equipment Heat Loads in ESF SWGR, DC SWBD,               2
2 J-105A-00013 MSFIS Information, Operation & Maintenance Manual
                  & Battery Rooms
W02 SY1503900 St andard Functional Description of System Medium Operated Isolation Valves
MISCELLANEOUS DOCUMENTS
W01  Main and Reheat Steam System
    NUMBER                                   TITLE                           REVISION /
18 STS EJ-100A RHR System Inservice Pump A Test
                                                                                  DATE
45 STS EN-100B Containment Spray Pump B Inservice Pump Test
ITLS Report 24045   Liquid Penetrant Inspection of Submitted Machined         August 7, 1978
26 TMP 11-013 ECCS Check Valve Leak Check
                    Parts
2 WCOP-02 Inser vice Testing Program Third
                    Jessop Steel Company - Ultrasonic Inspection Report       June 28, 1978
Ten-Year Interval
                    Operability Evaluation OE BB-12-004                             00
14  CALCULATIONS
Case N-616           Cases of ASME Boiler and Pressure Vessel Code             May 7, 1999
NUMBER TITLE REVISION AN 06-017 Steamline Break Core Response Analysis to Support MSIV/MFIV Replacement Project (DCP #09952)
SAP-12-58           Westinghouse LTR-SEE-III-12-81                           April 14, 2012
0 AN 06-018 Feedwater Line Break Analysis to Support the MSIV/MFIV Replacement Project (DCP
128136               Westinghouse Drawing Revision - Material Changes         September 28,
#09952) 0 AN-06-019 SGTR Stuck Open ARV Analysis to Support the MSIV/MFIV Replacement Project (DCP #09952)
                                                                                    1993
0 AN-06-020 Steam Generator Tube Rupture Overfill Analysis to Support the MSIV/MFIV Replacement Project (DCP #09952)
CA2412               1st & 2nd Off Check Valve PMs                             December 26,
0 EJ-100A Pump: PEJ01A: Group A   DRAWINGS NUMBER TITLE REVISION M-628-00140 MSIV System Medium Actuator Schematic
                                                                                    2008
W01 M630-00124 Standard Functional Description of System Medium Operated Isolation Valves
OE BB12-004         BB8397A/B CVCS Alternate Charging to Loop 4 Check               00
W01  CONDITION REPORTS
                    Valve
 
CA4790               Write PMC Work Request                                   December 26,
  A-11 51396 51995     Section 4OA1: Performance Indicator Verification
                                                                                    2008
PROCEDURES
CA4791               Revise AP 23F-001                                         December 26,
NUMBER TITLE REVISION STS BB-006 Reactor Coolant System Inventory Balance Using NPIS Computer 9 AP 26A-007 NRC Performance Indicators
                                                                                    2008
8 STS CH-025 Reactor Coolant Dose Equivalent Iodine Determination
CA4792               Update BID-CV-1                                           December 26,
MISCELLANEOUS
                                                                                    2008
DOCUMENTS NUMBER TITLE REVISION NEI 99-02 Regulatory Assessment Performance Indicator Guidelines
M-622.1 (Q)         Design Specifcation for Packaged Air Conditioning Units         9
Section 4OA2: Identification and Resolution of Problems
WORK REQUESTS
  MISCELLANEOUS DOCUMENTS
03611-87         00122-87
NUMBER TITLE REVISION / DATE 12-1119-L-01 50754 Final Report on Laboratory Evaluation of Failed Containment  
CONDITION REPORTS
Electrical Penetration As
00048493         00048494             00051530         003419               0052822
sembly ZNE274 Module A
                                              A-7
; Purchase Order No. 758996/0Pressurizer Heater Cables Found Burnt
 
May 8, 2012
WORK ORERS
WM 12-0013 Notification of Readiness for Inspection of Human Performance and Problem Identification and Resolution Safety Culture Themes for the Wolf Creek Generating Station
07-295490-000   08-309436-000       10-324925-000     10-327516-000 10-327516-001
May 7, 2012
10-324925-000   10-331280-000       10-327516-000     11-339107-001 11-339107-002
  Wolf Creek Station
11-339107-000   12-351057-000       00-223094-011
-Wide Fundamental Behaviors
Section 1R18: Plant Modifications
Mar 19, 2012
    NUMBER                                 TITLE                         REVISION /
  Corrective Action Recovering Monitoring Metrics
                                                                            DATE
May 2012 Corrective Action Recovering Monitoring Metrics
BMV0037         Furmanite Adapter Installation Evaluation                   00
September 2011 Letter No. SL
MPM LR-001     Leak Sealant Injection                                       7
-WC-2012-003 Transmittal of Summary of Results for RELAP ESW Waterhammer Analysis
WCN-00-001     Reedy Engineering, Inc. No 00-216961-000                     0
June 19, 2012 IIT 12-001 Comprehensive Event Safety Significance Assessment
ECW-119         Furmanite The Solutions Group                                 0
  P.1(c) WCNOC Activities Associated with Resolutions of NRC Cross-Cutting Aspect P.1(c)
DRAWINGS
June 6, 2012
    NUMBER                                 TITLE                         REVISION /
P.1(a) WCNOC Activities Associated with Resolution of NRC Cross
                                                                            DATE
-Cutting Aspect P.1(a)
M-240-00072     Valve Assembly - 2 IN Diaphragm Y Type, Globe 1522             3
June 6, 2012
                LB.C.S
 
                1974 ASME Code, Article NC-3000
  A-12 MISCELLANEOUS DOCUMENTS
                1986 ASME Code, NC-3229
NUMBER TITLE REVISION / DATE P.1(d) WCNOC Activities Associated with Resolution of NRC Cross
                1983 ASME Code, NC3232.2
-Cutting Aspect P.1(d)
Fig NC3329(g)-1 1986 Edition ASME Code
June 6, 2012  Corrective Action Backlog Reduction Initiative
MPM LR-001       Leak Sealant Injection                                         7
May 2012 AI 28A-006 Apparent Cause Evaluation
Change Package Furnmanite Adapter Fitting and BMV0037 Furmanite Repair         00
CONDITION REPORTS
013482
  15367 23032 26691 34455 51952 48182 48642 50807 50754 50809 51207 51290 51303 51408 51464 51429 51698 51952 53137 54278 Section 4OA5: Other Activities
ECW-119         Pressure Seal Calculation Sheet                               0
PROCEDURES
CONDITION REPORT
NUMBER TITLE REVISION AP 28A-100 Condition Reports
52992
16 ALR 00-037E CVCS HT Trace
WORK ORDERS
8 SYS BG-206 Boric Acid System Operation
10-333183-002   10-333183-009       11-346576-002     11-346576-003 11-346576-006
40 AI-22A-001 Operator Work Arounds/Operator Burdens/Control Room Deficiencies
11-346576-009   11-346576-010       11-346576-015     11-346576-017
10A AE-04-51 Provide feedwater and controls to the steam generator (startup feedpump)
                                            A-8
  DRAWINGS NUMBER TITLE REVISION M-12BG05 Piping & Instrumentation Diagram Checmical & Volume Control System
 
17  CALCULATION
Section 1R19: Postmaintenance Testing
NUMBER TITLE REVISION BG-M-051 0 QUICK HIT DETAIL REPORT
PROCEDURES
 
    NUMBER                                 TITLE                             REVISION
  A-13 1953     CONDITION REPORTS
MPE GK-003     Control Room and Class 1E A/C Units Preventive                   3A
  20709 20717 21039 27909 29602 30995 31129 31746 32129 34730 34065 34455 36600 39846 39847 39848 39849 39850 39851 39852 40714 43454 45218 48234 49551 50052 52151-01 5222-01 52447-01 52613-01 52580 52851 53024 53793-01 53791-01 54238 54239 54240   MISCELLANEOUS DOCUMENTS
                Maintenance Activity
NUMBER TITLE REVISION / DATE Page 15 0f 31
MPE GK-004     GK Unit Preparation for Work                                       4
Apparent Cause Evaluation Time
STS IC-500G     Channel Calibration DT/TAVG Instrumentation Loop 4               22A
SCCI P.1/c
STS IC-204A     Channel Operational Test of TAVG, dT and Pressurizer             17B
AL 28A-100 Cause Evaluations
                Pressure Protection Set Four
April 24, 2012
INC C-0026     7300 Lead/Lag Card (NLL0G01 Artwork Revisions 12)                 2A
SEL 2010-189 RIS 2005-20 Alignment Benchmark
INC C-0016     7300 Summing AMP Card (NSA1 and NSA2)                           10A
November 8 and 22, 2010
STS IC-502B     Channel Calibration of 7300 Process Pressurizer Pressure         16
  Change Package 013130
                Instrumentation
15  WC-NRC Component Design Bases Inspection NRC Inspection Report 05000482/2010007
STS IC-444     Channel Calibration NIS Power Range N-44                         11B
January 11, 2011 BLSE 578 File 7854 SNUPPS Project Diesel Generator Building Ventilation System Description
WORK ORDERS
March 27, 1974 BLSE-435 File 7850 SNUPPS Project Heating, Ventilation, and Air Conditioning Design Criteria
12-354805-003   11-348929-000     11-348929-002     11-348929-003     11-348929-004
  Maintenance Rule Expert Panel Meeting Minutes
11-348929-005   12-355385-001     12-355293-001     12-355293-004     12-355293-005
April 19, 2012
DRAWINGS
EDI 23M-250 Engineering Desktop Instruction Monitoring Perfo
    NUMBER                                 TITLE                             REVISION
rmance to Criteria and Goals
E-13GK13A       Schematic Diagram Class IE Electrical Equipment A/C Unit           6
3 K15-002 Audit 12-04-CAP Corrective Action Program
QCP-20-514     Eddy Current Examination Technique Sheet                         5C
May 21, 2012
                Eddy Current Calibration Summaries
  WORK ORDERS
WIP-M-761-     Interconnecting wiring diagram cabinet 04 SNUPPS Nuclear          00
  10-332371-009 10-332371-022 10-332371-038   PERFORMANCE IMPROVEMENT REQUESTS
02102-004-A-1   Power Plant Controls
 
WIP-M-761-     Interconnecting wiring diagram cabinet 04 SNUPPS Nuclear          00
  A-14 49220 42496
02088-W08-A-1   Power Plant Controls
M-761-02084     Interconnecting wiring diagram cabinet 04 SNUPPS Nuclear       W20
                Power Plant Controls
                                          A-9
 
Section 1R22: Surveillance Testing
PROCEDURES
    NUMBER                                 TITLE                         REVISION
ABHV0011       Solenoid Block Replacement
STS AB-205     Main Steam System Inservice Valve Test                       29
6101-00007     CS Innovations LLC 2008 Confidential and Proprietary         2
J-105A-00013   MSFIS Information, Operation & Maintenance Manual           W02
SY1503900       Standard Functional Description of System Medium           W01
                Operated Isolation Valves
                Main and Reheat Steam System                                 18
STS EJ-100A     RHR System Inservice Pump A Test                             45
STS EN-100B     Containment Spray Pump B Inservice Pump Test                 26
TMP 11-013     ECCS Check Valve Leak Check                                   2
WCOP-02         Inservice Testing Program Third Ten-Year Interval           14
CALCULATIONS
    NUMBER                                 TITLE                         REVISION
AN 06-017       Steamline Break Core Response Analysis to Support             0
                MSIV/MFIV Replacement Project (DCP #09952)
AN 06-018       Feedwater Line Break Analysis to Support the MSIV/MFIV       0
                Replacement Project (DCP #09952)
AN-06-019                                                                     0
                SGTR Stuck Open ARV Analysis to Support the MSIV/MFIV
                Replacement Project (DCP #09952)
AN-06-020       Steam Generator Tube Rupture Overfill Analysis to Support     0
                the MSIV/MFIV Replacement Project (DCP #09952)
EJ-100A         Pump: PEJ01A: Group A
DRAWINGS
    NUMBER                                 TITLE                         REVISION
M-628-00140     MSIV System Medium Actuator Schematic                       W01
M630-00124     Standard Functional Description of System Medium           W01
                Operated Isolation Valves
CONDITION REPORTS
                                          A-10
 
51396           51995
Section 4OA1: Performance Indicator Verification
PROCEDURES
    NUMBER                                 TITLE                           REVISION
STS BB-006     Reactor Coolant System Inventory Balance Using NPIS             9
                Computer
AP 26A-007     NRC Performance Indicators                                     8
STS CH-025     Reactor Coolant Dose Equivalent Iodine Determination           5
MISCELLANEOUS DOCUMENTS
    NUMBER                                 TITLE                           REVISION
NEI 99-02       Regulatory Assessment Performance Indicator Guidelines           6
Section 4OA2: Identification and Resolution of Problems
MISCELLANEOUS DOCUMENTS
    NUMBER                                 TITLE                           REVISION /
                                                                              DATE
12-1119-L-01   Final Report on Laboratory Evaluation of Failed Containment May 8, 2012
50754          Electrical Penetration Assembly ZNE274 Module A; Purchase
                Order No. 758996/0Pressurizer Heater Cables Found Burnt
WM 12-0013     Notification of Readiness for Inspection of Human           May 7, 2012
                Performance and Problem Identification and Resolution
                Safety Culture Themes for the Wolf Creek Generating Station
                Wolf Creek Station-Wide Fundamental Behaviors               Mar 19, 2012
                Corrective Action Recovering Monitoring Metrics               May 2012
                Corrective Action Recovering Monitoring Metrics             September
                                                                                2011
Letter No. SL- Transmittal of Summary of Results for RELAP ESW               June 19,
WC-2012-003    Waterhammer Analysis                                            2012
IIT 12-001     Comprehensive Event Safety Significance Assessment
P.1(c)         WCNOC Activities Associated with Resolutions of NRC         June 6, 2012
                Cross-Cutting Aspect P.1(c)
P.1(a)         WCNOC Activities Associated with Resolution of NRC Cross- June 6, 2012
                Cutting Aspect P.1(a)
                                          A-11
 
MISCELLANEOUS DOCUMENTS
    NUMBER                                 TITLE                           REVISION /
                                                                              DATE
P.1(d)         WCNOC Activities Associated with Resolution of NRC Cross- June 6, 2012
                Cutting Aspect P.1(d)
                Corrective Action Backlog Reduction Initiative           May 2012
AI 28A-006     Apparent Cause Evaluation                                       2
CONDITION REPORTS
15367           23032               26691             34455           51952
48182           48642               50807             50754           50809
51207           51290               51303             51408           51464
51429           51698               51952             53137           54278
Section 4OA5: Other Activities
PROCEDURES
    NUMBER                                 TITLE                           REVISION
AP 28A-100     Condition Reports                                               16
ALR 00-037E     CVCS HT Trace                                                   8
SYS BG-206     Boric Acid System Operation                                     40
AI-22A-001     Operator Work Arounds/Operator Burdens/Control Room           10A
                Deficiencies
AE-04-51       Provide feedwater and controls to the steam generator
                (startup feedpump)
DRAWINGS
    NUMBER                                 TITLE                           REVISION
M-12BG05       Piping & Instrumentation Diagram Checmical & Volume             17
                Control System
CALCULATION
    NUMBER                                 TITLE                           REVISION
BG-M-051                                                                         0
QUICK HIT DETAIL REPORT
                                          A-12
 
1953
CONDITION REPORTS
20709         20717             21039             27909               29602
30995         31129             31746             32129               34730
34065         34455             36600             39846               39847
39848         39849             39850             39851               39852
40714         43454             45218             48234               49551
50052         52151-01         5222-01           52447-01           52613-01
52580         52851             53024             53793-01           53791-01
54238         54239             54240
MISCELLANEOUS DOCUMENTS
    NUMBER                             TITLE                               REVISION /
                                                                              DATE
Page 15 0f 31 Apparent Cause Evaluation Time                                 SCCI P.1/c
AL 28A-100   Cause Evaluations                                           April 24, 2012
SEL 2010-189 RIS 2005-20 Alignment Benchmark                               November 8
                                                                            and 22, 2010
              Change Package 013130                                             15
              WC-NRC Component Design Bases Inspection NRC                   January 11,
              Inspection Report 05000482/2010007                               2011
BLSE 578     SNUPPS Project Diesel Generator Building Ventilation           March 27,
File 7854    System Description                                                1974
BLSE-435     SNUPPS Project Heating, Ventilation, and Air Conditioning
File 7850    Design Criteria
              Maintenance Rule Expert Panel Meeting Minutes               April 19, 2012
EDI 23M-250   Engineering Desktop Instruction Monitoring Performance to          3
              Criteria and Goals
K15-002       Audit 12-04-CAP Corrective Action Program                   May 21, 2012
WORK ORDERS
10-332371-009 10-332371-022     10-332371-038
PERFORMANCE IMPROVEMENT REQUESTS
                                      A-13
 
49220 42496
            A-14
}}
}}

Latest revision as of 22:18, 4 November 2019

IR 05000482/12-003, 03/31/2012 - 06/29/2012 for Wolf Creek Generating Station, Integrated Resident and Regional Report; Flood Protection Measures, Plant Modifications - Supersedes ML12219A181
ML13065A049
Person / Time
Site: Wolf Creek Wolf Creek Nuclear Operating Corporation icon.png
Issue date: 08/03/2012
From: O'Keefe N
NRC/RGN-IV/DNMS/NMSB-B
To: Matthew Sunseri
Wolf Creek
O'Keefe N
References
IR-12-003
Download: ML13065A049 (52)


See also: IR 05000482/2012003

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION I V

1600 EAST LAMAR BLVD

ARLINGTON, TEXAS 76011-4511

August 3, 2012

Matthew W. Sunseri, President and

Chief Executive Officer

Wolf Creek Nuclear Operating Corporation

P. O. Box 411

Burlington, KS 66839

SUBJECT: WOLF CREEK GENERATING STATION - INTEGRATED INSPECTION

REPORT 05000482/2012003

Dear Mr. Sunseri:

On June 29, 2012, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at

your Wolf Creek facility. The enclosed inspection report documents the inspection results which

were discussed on July 18, 2012, with Mr. Richard Clemens and other members of your staff.

The inspections examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

One NRC identified finding and one self-revealing finding of very low safety significance (Green)

were identified during this inspection. Both of these findings were determined to involve

violations of NRC requirements. Further, a licensee-identified violation which was determined to

be of very low safety significance is listed in this report. The NRC is treating these violations as

non-cited violations (NCVs) consistent with Section 2.3.2 of the Enforcement Policy.

If you contest these non-cited violations, you should provide a response within 30 days of the

date of this inspection report, with the basis for your denial, to the Nuclear Regulatory

Commission, ATTN: Document Control Desk, Washington DC 20555-0001; with copies to the

Regional Administrator, Region IV; the Director, Office of Enforcement, United States Nuclear

Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at the

Wolf Creek Generating Station.

If you disagree with a crosscutting aspect assignment in this report, you should provide a

response within 30 days of the date of this inspection report, with the basis for your

disagreement, to the Regional Administrator, Region IV; and the NRC Resident Inspector at the

Wolf Creek Generating Station.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its

enclosure, and your response (if any) will be available electronically for public inspection in the

NRC Public Document Room or from the Publicly Available Records (PARS) component of

NRC's Agencywide Document Access and Management System (ADAMS). ADAMS is

M. Suneri -2-

accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public

Electronic Reading Room).

Sincerely,

/RA/

Neil OKeefe, Chief

Project Branch B

Division of Reactor Projects

Docket No.: 05000482

License No: NPF-42

Enclosure: Inspection Report 05000482/2012003

w/ Attachment: Supplemental Information

cc w/ encl: Electronic Distribution

M. Suneri -3-

Electronic distribution by RIV:

Regional Administrator (Elmo.Collins@nrc.gov)

Deputy Regional Administrator (Art.Howell@nrc.gov)

DRP Director (Kriss.Kennedy@nrc.gov)

Acting DRP Deputy Director (Allen.Howe@nrc.gov)

Acting DRS Director (Tom.Blount @nrc.gov)

Acting DRS Deputy Director (Patrick.Louden@nrc.gov)

Senior Resident Inspector (Chris.Long@nrc.gov)

Resident Inspector (Charles.Peabody@nrc.gov)

WC Administrative Assistant (Shirley.Allen@nrc.gov)

Branch Chief, DRP/B (Neil.OKeefe@nrc.gov)

Senior Project Engineer, DRP/B (Leonard.Willoughby@nrc.gov)

Project Engineer, DRP/B (Nestor.Makris@nrc.gov)

Public Affairs Officer (Victor.Dricks@nrc.gov)

Public Affairs Officer (Lara.Uselding@nrc.gov)

Project Manager (Terry.Beltz@nrc.gov)

Acting Branch Chief, DRS/TSB (Dale.Powers@nrc.gov)

RITS Coordinator (Marisa.Herrera@nrc.gov)

Regional Counsel (Karla.Fuller@nrc.gov)

Congressional Affairs Officer (Jenny.Weil@nrc.gov)

OEMail Resource

DRS/TSB STA (Dale.Powers@nrc.gov)

Executive Technical Assistant (Silas.Kennedy@nrc.gov)

R:\_REACTORS\_WC\2012\2012003.docx

SUNSI Rev Compl. Yes No ADAMS Yes No Reviewer Initials NFO

Publicly Avail. Yes No Sensitive Yes No Sens. Type Initials NFO

SRI:DRP/B RI:DRP/B SPE:DRP/B C:DRS/EB1 C:DRS/EB2 C:DRS/OB

CLong CPeabody LWilloughby TFarnholtz GMiller MHaire

/NFO via E/ /NFO via E/ /RA via E/ /RA/ /RA/ /NFO via T/

7/20/12 7/20/12 8/9/12 7/31/12 7/31/12 8/1/12

C:DRS/PSB1 C:DRS/PSB2 AC:DRS/TSB BC:DRP/B

MHay JDrake RKellar NOKeefe

/RA/ /RA/ DPowers for /RA/

8/1/12 8/1/12 8/1/12 8/3/12

OFFICIAL RECORD COPY T=Telephone E=Email F=Fax

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket: 05000482

License: NPF-042

Report: 05000482/2012003

Licensee: Wolf Creek Nuclear Operating Corporation

Facility: Wolf Creek Generating Station

Location: 1550 Oxen Lane NE, Burlington, Kansas

Dates: March 31 through June 29, 2012

Inspectors: C. Long, Senior Resident Inspector

C. Peabody, Resident Inspector

N. Makris, Project Engineer

C. Alldredge, Health Physicist

N. Greene, PhD, Health Physicist

L. Carson II, Senior Health Physicist

J. ODonnell, Health Physicist

L. Ricketson, P.E., Senior Health Physicist

Approved Neil OKeefe, Chief, Project Branch B

By: Division of Reactor Projects

SUMMARY OF FINDINGS

IR 05000482/2012003; 03/31/2012 - 06/29/2012; Wolf Creek Generation Station, Integrated

Resident and Regional Report; Flood Protection Measures, Plant Modifications.

The report covered a 3-month period of inspection by resident inspectors and an announced

baseline inspection by region-based inspectors. Two Green noncited violations of significance

were identified. The significance of most findings is indicated by their color (Green, White,

Yellow, or Red) using Inspection Manual Chapter 0609, Significance Determination Process.

The crosscutting aspect is determined using Inspection Manual Chapter 0310, Components

Within the Cross Cutting Areas. Findings for which the significance determination process

does not apply may be Green or be assigned a severity level after NRC management review.

The NRC's program for overseeing the safe operation of commercial nuclear power reactors is

described in NUREG-1649, Reactor Oversight Process, Revision 4, dated December 2006.

A. NRC-Identified Findings and Self-Revealing Findings

Cornerstone: Initiating Events

Appendix B, Criterion V, Instructions, Procedures, and Drawings, for a work

order that did not accomplish a leak seal repair in accordance with its

engineering evaluation. Valve BMV0037 is a safety related ASME Code Class 2

steam generator blowdown valve that had a body-to-bonnet steam leak. Wolf

Creek and its vendor produced modification documents to perform a leak-seal

repair. The inspectors identified that on December 10, 2011, Wolf Creek installed

an injection port in the valve body in close proximity of another injection port.

Work orders allowed the location of the injection ports to be determined by the

work. The pair was not installed in accordance with change package 9385. After

inspector questioning, Wolf Creek performed an evaluation that demonstrated

that the valve body retained structural integrity. This issue was entered into the

corrective action program under condition report 52992.

The failure to ensure that the configuration of a safety-related steam generator

blowdown was controlled in accordance with the approved engineering change

package during leak seal activities is a performance deficiency. This finding was

more than minor because it impacted the procedure quality attribute of the

Initiating Events Cornerstone and affected the objective to limit the likelihood of

those events that upset plant stability and challenge critical safety functions

during shutdown as well as power operations. Using Inspection Manual Chapter 0609, Appendix A, this finding was determined to be of very low safety

significance because an evaluation after the modification was able to

demonstrate structural integrity. Therefore, the finding does not contribute to both

the likelihood of a reactor trip and the likelihood that mitigation equipment will not

be available. The inspectors identified the cause of the finding had a human

performance crosscutting aspect in the area of resources. Specifically, the

licensee did not ensure that the work order instructions were complete, accurate,

and reflected up-to-date design documentation sufficiently to control plant

configuration in accordance with design H.2.c] (Section 1R18).

-2- Enclosure

Cornerstone: Mitigating Systems

Criterion V, Inspections, Procedures, and Drawings, was identified as a result of

a leaking watertight door that was observed on January 13, 2012. Station

procedure MPM XX-002, Watertight Door Preventive Maintenance Activities,

failed to ensure the proper position of the alignment screws, which resulted in

leakage through a misalignment between the door and its threshold. During the

January 13, 2012, loss of offsite power, the auxiliary building general area sump

pumps did not operate for approximately 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />. Condensed steam and other

effluents slowly accrued in the stairwell area outside the containment spray pump

rooms to a depth of 24 to 36 inches. The train B containment spray pump room

watertight door leaked approximately 10 gallons per minute and pooled in both

the containment spray pump room and the residual heat removal pump room to a

depth of three inches. This issue was entered into the corrective action program

under condition report 51622. The licensee corrected the procedure and

realigned the affected watertight doors.

Failure to properly adjust safety-related watertight door alignment screws during

testing activities is a performance deficiency. The performance deficiency is

more than minor and therefore a finding because, if left uncorrected it could lead

to a more significant safety concern. Using Inspection Manual Chapter 0609,

Appendix A, the finding was characterized using Exhibit 4, Seismic, Flooding,

and Severe Weather Screening Criteria. The finding was determined to be of

very low safety significance (Green) because the degraded flood protection

equipment would not have caused a plant trip or other initiating event, would not

degrade two or more trains of a multi-train safety system, would not degrade one

or more trains of a supporting system, and the finding does not involve the total

loss of any safety function. The inspectors determined the cause of this finding

was not indicative of current performance. (Section 1R06).

B. Licensee-Identified Violations

A violation of very low safety significance was identified by the licensee and has been

reviewed by the inspectors. Corrective actions taken or planned by the licensee have

been entered into the licensees corrective action program. This violation and

associated corrective action tracking numbers are listed in Section 4OA7 of this report.

-3- Enclosure

REPORT DETAILS

Summary of Plant Status

Wolf Creek began the inspection period on March 31 at 100 percent power and remained at full

power until May 24, when power was reduced to 69 percent for planned turbine thermal

performance testing. Wolf Creek returned to 100 percent power later on May 24. On June 6,

Wolf Creek reduced power to 88 percent when it entered Limiting Condition of Operation 3.0.3

due to having the train A vital switchgear and battery air conditioning unit inoperable. Wolf

Creek returned to 100 percent power later on June 6 and remained at 100 percent for the rest of

the inspection period.

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection (71111.01)

.1 Readiness for Impending Adverse Weather Conditions

a. Inspection Scope

Since thunderstorms with potential tornados and high winds were forecast in the vicinity

of the facility for April 14, 2012, the inspectors reviewed the plant personnels overall

preparations/protection for the expected weather conditions. On April 13, 2012, the

inspectors walked down the condensate storage tank, demineralized water storage tank,

reactor makeup water, and refueling water storage tank because their functions could be

affected, or required, as a result of high winds or tornado-generated missiles or the loss

of offsite power. The inspectors evaluated the plant staffs preparations against the sites

procedures and determined that the staffs actions were adequate. During the

inspection, the inspectors focused on plant-specific design features and the licensees

procedures used to respond to specified adverse weather conditions. The inspectors

also toured the plant grounds to look for any loose debris that could become missiles

during a tornado. The inspectors evaluated operator staffing and accessibility of

controls and indications for those systems required to control the plant. Additionally, the

inspectors reviewed the Updated Safety Analysis Report (USAR) and performance

requirements for the systems selected for inspection, and verified that operator actions

were appropriate as specified by plant-specific procedures. The inspectors also

reviewed a sample of corrective action program items to verify that the licensee-

identified adverse weather issues at an appropriate threshold and dispositioned them

through the corrective action program in accordance with station corrective action

procedures. Specific documents reviewed during this inspection are listed in the

attachment.

Because the storm of April 14, 2012, caused the temporary diesel-driven fire water pump

to be locally shut down due to wave action on Coffey County lake, and a second storm

with similar behavior was predicted to arrive on April 19, the inspectors reviewed

corrective action documents and the temporary fire pump operating procedures. The

inspectors discussed applicable equipment and staffing requirements with the operations

-4- Enclosure

superintendent. The inspectors reviewed plans to secure the pump during periods of

high wave action for the long-term safety and reliability of the pump, and to have the

dedicated operator stationed in an adjacent building to restart the pump in the event of

an actual fire. The inspectors reviewed station procedures for operation of the

temporary diesel-driven fire water pump and walked down the pump, as well as the

suction, and discharge system connection. The inspectors also walked down the electric

motor-driven fire water pump and service water pumps in the adjacent circulating water

screen house building to verify that the area was free from any wind-driven missiles and

that the equipment would be available to respond to a valid demand in the event of a

fire. Specific documents reviewed are listed in the attachment.

These activities constitute completion of two readiness for impending adverse weather

condition samples as defined in Inspection Procedure 71111.01-05.

b. Findings

No findings were identified.

.2 Summer Readiness for Offsite and Alternate-ac Power

a. Inspection Scope

The inspectors performed a review of preparations for summer weather for selected

systems, including conditions that could lead to loss-of-offsite power and conditions that

could result from high temperatures. The inspectors reviewed the procedures affecting

these areas and the communications protocols between the transmission system

operator and the plant to verify that the appropriate information was being exchanged

when issues arose that could affect the offsite power system. Examples of aspects

considered in the inspectors review included:

  • The coordination between the transmission system operator and the plants

operations personnel during off-normal or emergency events

  • The explanations for the events
  • The estimates of when the offsite power system would be returned to a normal

state

  • The notifications from the transmission system operator to the plant when the

offsite power system was returned to normal

During the inspection, the inspectors focused on plant-specific design features and the

procedures used by plant personnel to mitigate or respond to adverse weather

conditions. Additionally, the inspectors reviewed the USAR and performance

requirements for systems selected for inspection, and verified that operator actions were

appropriate as specified by plant-specific procedures. Specific documents reviewed

during this inspection are listed in the attachment. The inspectors also reviewed

corrective action program items to verify that the licensee was identifying adverse

-5- Enclosure

weather issues at an appropriate threshold and entering them into their corrective action

program in accordance with station corrective action procedures.

These activities constitute completion of one readiness for summer weather affect on

offsite and alternate-ac power sample as defined in Inspection Procedure 71111.01-05.

b. Findings

No findings were identified.

1R04 Equipment Alignment (71111.04)

Partial Walkdown

a. Inspection Scope

The inspectors performed partial system walkdowns of the following risk-significant

systems:

  • April 14, 2012, Auxiliary building watertight doors and internal flood barriers with

train B emergency core cooling watertight door out of service

  • June 19, 2012, Boron injection tank depressurization flowpath through the safety

injection test line

The inspectors selected these systems based on their risk significance relative to the

Reactor Safety Cornerstones at the time they were inspected. The inspectors attempted

to identify any discrepancies that could affect the function of the system, and, therefore,

potentially increase risk. The inspectors reviewed applicable operating procedures,

system diagrams, USAR, technical specification requirements, administrative technical

specifications, outstanding work orders, condition reports, and the impact of ongoing

work activities on redundant trains of equipment in order to identify conditions that could

have rendered the systems incapable of performing their intended functions. The

inspectors also inspected accessible portions of the systems to verify system

components and support equipment were aligned correctly and operable. The

inspectors examined the material condition of the components and observed operating

parameters of equipment to verify that there were no obvious deficiencies. The

inspectors also verified that the licensee had properly identified and resolved equipment

alignment problems that could cause initiating events or impact the capability of

mitigating systems or barriers and entered them into the corrective action program with

the appropriate significance characterization. Specific documents reviewed during this

inspection are listed in the attachment.

These activities constitute completion of two partial system walkdown samples as

defined in Inspection Procedure 71111.04-05.

b. Findings

No findings were identified.

-6- Enclosure

1R05 Fire Protection (71111.05)

Quarterly Fire Inspection Tours

a. Inspection Scope

The inspectors conducted fire protection walkdowns that were focused on availability,

accessibility, and the condition of firefighting equipment in the following risk-significant

plant areas:

The inspectors reviewed areas to assess if licensee personnel had implemented a fire

protection program that adequately controlled combustibles and ignition sources within

the plant; effectively maintained fire detection and suppression capability; maintained

passive fire protection features in good material condition; and had implemented

adequate compensatory measures for out of service, degraded or inoperable fire

protection equipment, systems, or features, in accordance with the licensees fire plan.

The inspectors selected fire areas based on their overall contribution to internal fire risk

as documented in the plants Individual Plant Examination of External Events with later

additional insights, their potential to affect equipment that could initiate or mitigate a

plant transient, or their impact on the plants ability to respond to a security event. Using

the documents listed in the attachment, the inspectors verified that fire hoses and

extinguishers were in their designated locations and available for immediate use; that

fire detectors and sprinklers were unobstructed; that transient material loading was

within the analyzed limits; and fire doors, dampers, and penetration seals appeared to

be in satisfactory condition. The inspectors also verified that minor issues identified

during the inspection were entered into the licensees corrective action program.

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of three quarterly fire-protection inspection

samples as defined in Inspection Procedure 71111.05-05.

b. Findings

No findings were identified.

1R06 Flood Protection Measures (71111.06)

a. Inspection Scope

The inspectors reviewed the USAR, the flooding analysis, and plant procedures to

assess susceptibilities involving internal flooding; reviewed the corrective action program

to determine if licensee personnel identified and corrected flooding problems; inspected

underground bunkers/manholes to verify the adequacy of sump pumps, level alarm

circuits, cable splices subject to submergence, and drainage for bunkers/manholes; and

-7- Enclosure

verified that operator actions for coping with flooding can reasonably achieve the desired

outcomes. The inspectors also inspected the areas listed below to verify the adequacy

of equipment seals located below the flood line, floor and wall penetration seals,

watertight door seals, common drain lines and sumps, sump pumps, level alarms, and

control circuits, and temporary or removable flood barriers. Specific documents

reviewed during this inspection are listed in the attachment.

pump rooms

These activities constitute completion of one flood protection measures inspection

sample as defined in Inspection Procedure 71111.06-05.

b. Findings

Introduction. A Green, self-revealing, non-cited violation of 10 CFR 50, Appendix B,

Criterion V, Inspections, Procedures, and Drawings, was identified as a result of a

leaking watertight door that was observed on January 13, 2012. Station Procedure

MPM XX-002 Watertight Door Preventive Maintenance Activities, failed to ensure the

proper position of the alignment screws, which resulted in leakage through a

misalignment between the door and its threshold.

Description. On January 13, 2012, Wolf Creek tripped due to a main generator breaker

fault. Many non-safety systems were without power for several days until temporary

power could be arranged. One such system was the auxiliary building general area

sumps, which were without power for approximately 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />. Condensed steam and

other effluents slowly accrued in the stairwell area outside the containment spray pump

rooms. The containment spray pump rooms lead to the corresponding train residual

heat removal pump rooms. Each train of containment spray pump rooms is separated

from the stairwell by a watertight door. There is no flood protection between the

corresponding containment spray and residual heat removal pump rooms. Over the

36-hour period without power, the general area water level rose to approximately 24 to

30 inches in depth, which was above the bottom of the watertight doors. The train A

containment spray pump room door passed minimal leakage with no impact to

safety-related equipment in the rooms. The train B containment spray pump room door

passed an unacceptable amount of leakage estimated to be approximately 10 gpm and

pooled into both the containment spray pump room and the residual heat removal pump

room to a depth of three inches.

On April 17, 2012, Wolf Creek identified that a previous condition report screening

resulted in a nonconservative operability assessment of door leakage. The licensee

discovered that corrective actions had not been taken and at 2:53 p.m., control room

operators promptly declared the door and the train B containment spray and train B

residual heat removal pumps inoperable and entered the appropriate technical

specification action statements. The licensee inspected the material condition of the

gasket and determined that it met the requirements of its preventive maintenance activity

detailed in station procedure MPM XX-002, Watertight Doors Preventive Maintenance

Activity. At that point, the licensee determined that the procedure must be in some way

inadequate. The licensee contacted another facility for information and compared their

-8- Enclosure

respective procedures. The licensee determined that another facility was regularly

adjusting the doors alignment screws (dog ears) whereas Wolf Creeks procedure

directed the mechanic to skip that step if the door passed its chalk test in the previous

step.

The chalk test checks engagement between the door frame and the door seal.

Operations personnel determined that the chalk test had a high likelihood of producing a

false positive because the chalk is transferred around the entire perimeter of the seal

when the mechanic closes the door, appearing to demonstrate a proper seal. However,

actual sealing occurs when the hand wheel is turned to engage the dog ears. If the dog

ears are properly aligned, the door will seal around the entire seating surface. However,

if they are loose, the door may rest ajar in the threshold allowing water to pass. A field

inspection observed that six of eight dog ears were loose on the containment spray room

B watertight door, whereas only two of eight dog ears on the train A door were loose and

it performed satisfactorily under the same flood conditions. The licensee completed the

adjustments of the to the alignment screws, door jamb welding, and seal replacement

and returned the train B containment spray and emergency core cooling systems to

service at 2:48 p.m. on April 18, 2011.

Analysis. Failure to properly adjust safety-related watertight door alignment screws

during testing activities is a performance deficiency. The performance deficiency is

more than minor, and therefore a finding because, if left uncorrected it could lead to a

more significant safety concern. Using Inspection Manual Chapter 0609, Appendix A,

the finding was characterized under the Exhibit 4, Seismic, Flooding, and Severe

Weather Screening Criteria. The finding was determined to be of very low safety

significance (Green) because the degraded flood protection equipment would not have

caused a plant trip or other initiating event, would not degrade two or more trains of a

multi-train safety system, would not degrade one or more trains of a supporting system,

and the finding does not involve the total loss of any safety function. The inspectors

determined the cause of this finding was not indicative of current performance.

Enforcement. Title 10 CFR 50, Appendix B, Criterion V, states that: Activities affecting

quality shall be prescribed by documented instructions, procedures, or drawings of a

type appropriate to the circumstances and shall be accomplished in accordance with

these instructions, procedures, or drawings. Instructions, procedures, or drawings shall

include appropriate quantitative or qualitative acceptance criteria for determining that

important activities have been satisfactorily accomplished. Procedure MPM XX-002,

Watertight Doors Preventive Maintenance Activity, Revision 4, a safety-related

procedure, was intended to implement activities affecting quality for flood doors.

Contrary to the above, from original plant construction in 1985 through April 18, 2012,

the licensee performed activities affecting the quality of watertight doors using a

procedure that was not appropriate to the circumstances. Specifically, Wolf Creek

station procedure MPM XX-002, Watertight Doors Preventive Maintenance Activity,

Revision 4, failed to ensure the proper position of the door alignment screws, which

resulted in leakage due to misalignment. Because this finding is of very low safety

significance and was entered into the licensee corrective action program as condition

report 51622, this violation is being treated as a non-cited violation in accordance with

Section 2.3.2 of the Enforcement Policy: NCV 05000482/2012003-01, Unacceptable

Leakage Through Safety-Related Watertight Door During Loss of Offsite Power.

-9- Enclosure

1R11 Licensed Operator Requalification Program and Licensed Operator Performance

(71111.11)

.1 Quarterly Review of Licensed Operator Requalification Program

a. Inspection Scope

On June 18, 2012, the inspectors observed a crew of licensed operators in the plants

simulator during requalification testing. The inspectors assessed the following areas:

  • Licensed operator performance
  • The ability of the licensee to administer the evaluations
  • The modeling and performance of the control room simulator
  • The quality of post-scenario critiques
  • Followup actions taken by the licensee for identified discrepancies

These activities constitute completion of one quarterly licensed operator requalification

program sample as defined in Inspection Procedure 71111.11.

b. Findings

No findings were identified.

.2 Quarterly Observation of Licensed Operator Performance

a. Inspection Scope

On the evening of April 5, 2012, the inspectors observed the performance of on-shift

licensed operators in the plants main control room. At the time of the observations, the

plant was in a period of heightened activity due to Security Force on Force drills being

conducted throughout the plant. The inspectors observed the operators performance of

the following activities:

  • Shift turnover brief
  • Drill communication brief
  • Routine reactivity manipulations.

In addition, the inspectors assessed the operators adherence to plant procedures,

including procedure AP 21-001, Conduct of Operations, and other operations

department policies.

These activities constitute completion of one quarterly licensed-operator performance

sample as defined in Inspection Procedure 71111.11.

b. Findings

No findings were identified.

- 10 - Enclosure

1R12 Maintenance Effectiveness (71111.12)

a. Inspection Scope

The inspectors evaluated degraded performance issues involving the following risk

significant systems:

  • May 15, 2012, Startup main feedwater pump performance monitoring,

maintenance rule function AE-04

function SP-02

The inspectors reviewed events such as where ineffective equipment maintenance has

resulted in valid or invalid automatic actuations of engineered safeguards systems and

independently verified the licensee's actions to address system performance or condition

problems in terms of the following:

  • Implementing appropriate work practices
  • Identifying and addressing common cause failures
  • Characterizing system reliability issues for performance monitoring
  • Charging unavailability for performance monitoring
  • Trending key parameters for condition monitoring
  • Verifying appropriate performance criteria for structures, systems, and

components classified as having an adequate demonstration of performance

through preventive maintenance, as described in 10 CFR 50.65(a)(2), or as

requiring the establishment of appropriate and adequate goals and corrective

actions for systems classified as not having adequate performance, as described

in 10 CFR 50.65(a)(1)

The inspectors assessed performance issues with respect to the reliability, availability,

and condition monitoring of the system. In addition, the inspectors verified maintenance

effectiveness issues were entered into the corrective action program with the appropriate

significance characterization. Specific documents reviewed during this inspection are

listed in the attachment.

These activities constitute completion of two quarterly maintenance effectiveness

samples as defined in Inspection Procedure 71111.12-05.

- 11 - Enclosure

b. Findings

No findings were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

a. Inspection Scope

The inspectors reviewed licensee personnel's evaluation and management of plant risk

for the maintenance and emergent work activities affecting risk-significant and safety-

related equipment listed below to verify that the appropriate risk assessments were

performed prior to removing equipment for work:

  • April 10 and 15, 2012, NK02 DC bus voltage and current fluctuations

The inspectors selected these activities based on potential risk significance relative to

the Reactor Safety Cornerstones. As applicable for each activity, the inspectors verified

that licensee personnel performed risk assessments as required by 10 CFR 50.65(a)(4)

and that the assessments were accurate and complete. When licensee personnel

performed emergent work, the inspectors verified that the licensee personnel promptly

assessed and managed plant risk. The inspectors reviewed the scope of maintenance

work, discussed the results of the assessment with the licensee's probabilistic risk

analyst or shift technical advisor, and verified plant conditions were consistent with the

risk assessment. The inspectors also reviewed the technical specification requirements

and inspected portions of redundant safety systems, when applicable, to verify risk

analysis assumptions were valid and applicable requirements were met. Specific

documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of one maintenance risk assessments and

emergent work control inspection sample as defined in Inspection

Procedure 71111.13-05.

b. Findings

No findings were identified.

1R15 Operability Evaluations and Functionality Assessments (71111.15)

a. Inspection Scope

The inspectors reviewed the following issues:

  • April 13, 2012, Chemical and volume control system alternate charging line

check valves BBV8379A and BBV8379B potential stud degradation

  • April 18, 2012, Flood door operability in Auxiliary Building

181

- 12 - Enclosure

  • May 23, 2012, Refueling water storage tank valve BNV-11 manual actions during

sump recirculation

  • June 16, 2012, Vital Switchgear room temperatures after loss of train B air

conditioning unit

non-vital power loss with normal service water running in Mode 5

The inspectors selected these potential operability issues based on the risk significance

of the associated components and systems. The inspectors evaluated the technical

adequacy of the evaluations to ensure that technical specification operability was

properly justified and the subject component or system remained available such that no

unrecognized increase in risk occurred. The inspectors compared the operability and

design criteria in the appropriate sections of the technical specifications and USAR to

the licensee personnels evaluations to determine whether the components or systems

were operable. Where compensatory measures were required to maintain operability,

the inspectors determined whether the measures in place would function as intended

and were properly controlled. The inspectors determined, where appropriate,

compliance with bounding limitations associated with the evaluations. Additionally, the

inspectors also reviewed a sampling of corrective action documents to verify that the

licensee was identifying and correcting any deficiencies associated with operability

evaluations. Specific documents reviewed during this inspection are listed in the

attachment.

These activities constitute completion of six operability evaluation inspection samples as

defined in Inspection Procedure 71111.15-05.

b. Findings

No findings were identified.

1R18 Plant Modifications (71111.18)

Temporary Modifications

a. Inspection Scope

To verify that the safety functions of important safety systems were not degraded, the

inspectors reviewed the temporary modification for leak seal repair of steam generator

tube sheet drain valve BMV0037.

The inspectors reviewed the temporary modification and the associated safety-

evaluation screening against the system design bases documentation, including the

USAR and the technical specifications, and verified that the modification did not

adversely affect the system operability/availability. The inspectors also verified that the

installation and restoration were consistent with the modification documents and that

configuration control was adequate. Additionally, the inspectors verified that the

- 13 - Enclosure

temporary modification was identified on control room drawings, appropriate tags were

placed on the affected equipment, and licensee personnel evaluated the combined

effects on mitigating systems and the integrity of radiological barriers.

These activities constitute completion of one sample for temporary plant modifications as

defined in Inspection Procedure 71111.18-05.

b. Findings

Introduction. The inspectors identified a Green non-cited violation of 10 CFR Part 50,

Appendix B, Criterion V, Instructions, Procedures, and Drawings, for a work order that

did not accomplish a leak seal repair in accordance with its engineering evaluation.

Description. Valve BMV0037 is a 2-inch safety-related ASME Code Class 2 valve that

isolates the steam generator B tube sheet drain. This diaphragm type valve is not

required to change position but it is required to be a pressure boundary for the

secondary side of the steam generator. This safety-related quality valve is normally

closed and cannot be isolated from the steam generator.

On September 9, 2010, Wolf Creek experienced a leak at the body-to-bonnet joint for

valve BMV0037. Wolf Creek engineering utilized a previously approved a leak seal

repair using configuration change package 9385. Change package 13482 re-approved

change package 9385 for use. This change package approved drilling injection ports

into the valve body. On September 30, 2010, Wolf Creek and its contractor drilled two

injection ports 180 degrees apart on valve BMV0037 and injected leak sealant. From

September 30, 2010, to November 30, 2011, valve BMV0037 leaked and was injected

four times. On December 5, 2011, BMV0037 began leaking again and a third injection

port was installed.

The inspectors selected the inspection because the valve had leaked multiple times and

was not replaced. The inspectors made a containment entry on March 27, 2012, and

observed the sealant injection. The inspectors observed two injection ports drilled at

angles to the valve body in close proximity to one another and a third approximately 180

degrees on the other side of the valve body. Two of the injection ports were visually

estimated at three quarters of an inch apart and at a shallow angle to the valve body.

Valve BMV0037 was injected again on March 28, 2012, and May 8, 2012.

The inspectors reviewed work order 10-333183-002 that was used on September 30,

2010, to install the injection ports. The inspectors found no instructions in work

order 10-333183-002 for the orientation of the drilling for the injection ports, although

they were drilled 180 degrees apart. Step 1.7.5 of work order 10-333183-002 stated that

the activity was not to exceed three injection ports. The inspectors reviewed work

order 11-346576-006, which installed a third injection port on December 10, 2011,

adjacent to one of the existing injection ports. The inspectors noted that Step 1.8.4 of

work order 11-346576-006 allowed the location of the third injection port to be

determined by the vendor technician, and also noted that the third injection port was not

installed in accordance with change package 9385.

- 14 - Enclosure

The inspectors concluded that, despite repeated re-injections, Wolf Creek did not

exceed the evaluated limits for the amount of sealant allowed to be injected. However,

the inspectors noted that Wolf Creeks leak seal process did not require a valve with a

temporary leak seal repair to be replaced at the next outage, and it did not include a

caution that cooling down a hot system was likely to cause changes in the sealant

properties and result in another leak. The inspectors questioned why the valve was not

replaced during the previous refueling outage or the forced outage and were told that

Wolf Creek had had difficulty locating a replacement valve.

The inspectors reviewed configuration change packages 13482 and 9385. The

inspectors noted that configuration change package 9385 stated that three injection

ports shall be installed 120 degrees apart around the circumference of the valve body.

The holes for those injection ports were said not to require reinforcement because ASME

Code Section III, NC-3332.1 does not require reinforcement since the injection ports are

less than 2-inch nominal pipe size. ASME Code Section III, article NC-3300 is for

pressure vessels. The inspectors, with assistance from the Office of Nuclear Reactor

Regulation, determined that the use of article NC-3300 was reasonable, but the

application of article NC-3332.1 was not appropriate for multiple openings in a valve

body. The inspectors questioned if the reinforcement requirements of article NC-3330

were met. Wolf Creek subsequently evaluated the article NC-3330 reinforcement criteria

using dimensions reasonably estimated from a photo and the manufacturers valve

drawing. The inspectors concluded that the evaluation did not include the angles of the

injection ports. Drilling the injection ports at an angle other than 90 degrees (to the valve

body) results in a deeper hole to reach the body-to-bonnet threaded joint (the area

where the sealant was injected). This required more surrounding re-enforcement

material. The inspectors again questioned the loss of material, this time due to the

additional material lost to the injection port angles. Wolf Creek subsequently took actual

measurements during a containment entry and re-performed the ASME Code evaluation.

The evaluation considered the angled injection ports to be oval shaped holes through

the wall of the valve body per article NC-3331(a). This increased the amount of material

required for reinforcement. The inspectors reviewed the calculation and concluded that

the reinforcement requirements were met.

Analysis. The failure to ensure that the configuration of a safety-related steam generator

blowdown valve was controlled in accordance with the approved engineering change

package during leak seal activities is a performance deficiency. This finding was more

than minor because it impacted the procedure quality attribute of the Initiating Events

Cornerstone, and it affected the objective to limit the likelihood of those events that upset

plant stability and challenge critical safety functions during shutdown as well as power

operations. Using Inspection Manual Chapter 0609, Appendix A, The Significance

Determination Process (SDP) for Findings At-Power, this finding was determined to be

of very low safety significance because an evaluation after the modification was able to

demonstrate structural integrity. Therefore, the finding does not contribute to both the

likelihood of a reactor trip and the likelihood that mitigation equipment will not be

available. The inspectors identified the cause of the finding had a in the human

performance crosscutting aspect in the area of resources. Specifically, the licensee did

not ensure that the work order instructions were sufficiently complete, accurate and

reflected up-to-date design documentation sufficient to control plant configuration in

accordance with design H.2.c.

- 15 - Enclosure

Enforcement. Title 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures,

and Drawings, requires, in part, that activities affecting quality shall be prescribed by

documented instructions, procedures, or drawings, of a type appropriate to the

circumstances and shall be accomplished in accordance with these instructions,

procedures, or drawings. Instructions, procedures, or drawings shall include acceptance

criteria for determining that activities have been satisfactorily accomplished. Wolf Creek

configuration change package 9385 allowed up to three injection ports 120 degrees

apart on the valve body. Contrary to the above, on September 30, 2010, the licensee

performed an activity affecting quality using documented instructions that were not

appropriate to the circumstances. Work order 10-333183-002 contained no instructions

for the modification of the safety-related valve BMV0037 by installing injection ports.

Specifically, there were no instructions or acceptance criteria for injection port positioning

or orientation, even though the position and orientation to the drilled holes affect the

structural integrity of the valve body. Because this issue was determined to be of very

low safety significance (Green) and was entered into the licensees corrective action

program as condition report 52992, this violation is being treated as a non-cited violation

in accordance with Section VI.A.1 of the NRC Enforcement Policy: NCV 05000482/2012003-02, Incorrect Leak Seal Injection Port Installation.

1R19 Post Maintenance Testing (71111.19)

a. Inspection Scope

The inspectors reviewed the following postmaintenance activities to verify that

procedures and test activities were adequate to ensure system operability and functional

capability:

  • May 31, 2012, Vital switchgear cooler SGK05B after compressor replacement
  • June 18-25, 2012, Over-temperature delta-temperature circuit card replacements

The inspectors selected these activities based upon the structure, system, or

component's ability to affect risk. The inspectors evaluated these activities for the

following (as applicable):

  • The effect of testing on the plant had been adequately addressed; testing was

adequate for the maintenance performed

  • Acceptance criteria were clear and demonstrated operational readiness; test

instrumentation was appropriate

The inspectors evaluated the activities against the technical specifications, the USAR,

10 CFR Part 50 requirements, licensee procedures, and various NRC generic

communications to ensure that the test results adequately ensured that the equipment

met the licensing basis and design requirements. In addition, the inspectors reviewed

corrective action documents associated with postmaintenance tests to determine

whether the licensee was identifying problems and entering them in the corrective action

program and that the problems were being corrected commensurate with their

- 16 - Enclosure

importance to safety. Specific documents reviewed during this inspection are listed in

the attachment.

These activities constitute completion of three postmaintenance testing inspection

samples as defined in Inspection Procedure 71111.19-05.

b. Findings

No findings were identified.

1R22 Surveillance Testing (71111.22)

a. Inspection Scope

The inspectors reviewed the USAR, procedure requirements, and technical

specifications to ensure that the surveillance activities listed below demonstrated that the

systems, structures, and/or components tested were capable of performing their

intended safety functions. The inspectors either witnessed or reviewed test data to

verify that the significant surveillance test attributes were adequate to address the

following:

  • Preconditioning
  • Evaluation of testing impact on the plant
  • Acceptance criteria
  • Test equipment
  • Procedures
  • Jumper/lifted lead controls
  • Test data
  • Testing frequency and method demonstrated technical specification operability
  • Test equipment removal
  • Restoration of plant systems
  • Fulfillment of ASME Code requirements
  • Updating of performance indicator data
  • Engineering evaluations, root causes, and bases for returning tested systems,

structures, and components not meeting the test acceptance criteria were correct

- 17 - Enclosure

  • Reference setting data

The inspectors also verified that licensee personnel identified and implemented any

needed corrective actions associated with the surveillance testing.

  • June 10, 2012, Spent fuel pool pump B inservice testing

system check valve leak test

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of six surveillance testing inspection samples as

defined in Inspection Procedure 71111.22-05.

b. Findings

No findings were identified.

2. RADIATION SAFETY

Cornerstone: Occupational and Public Radiation Safety

2RS05 Radiation Monitoring Instrumentation (71124.05)

a. Inspection Scope

This area was inspected to verify the licensee is assuring the accuracy and operability of

radiation monitoring instruments that are used to: (1) monitor areas, materials, and

workers to ensure a radiologically safe work environment and (2) detect and quantify

radioactive process streams and effluent releases. The inspectors used the

requirements in 10 CFR Part 20, the technical specifications, and the licensees

procedures required by technical specifications as criteria for determining compliance.

During the inspection, the inspectors interviewed licensee personnel, performed

walkdowns of various portions of the plant, and reviewed the following items:

- 18 - Enclosure

  • Selected plant configurations and alignments of process, post-accident, and

effluent monitors with descriptions in the USAR and the offsite dose calculation

manual

  • Select instrumentation, including effluent monitoring instrument, portable survey

instruments, area radiation monitors, continuous air monitors, personnel

contamination monitors, portal monitors, and small article monitors to examine

their configurations and source checks

  • Calibration and testing of process and effluent monitors, laboratory

instrumentation, whole body counters, post-accident monitoring instrumentation,

portal monitors, personnel contamination monitors, small article monitors,

portable survey instruments, area radiation monitors, electronic dosimetry, air

samplers, continuous air monitors

  • Audits, self-assessments, and corrective action documents related to radiation

monitoring instrumentation since the last inspection

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of the one required sample as defined in

Inspection Procedure 71124.05-05.

b. Findings

No findings were identified.

2RS06 Radioactive Gaseous and Liquid Effluent Treatment (71124.06)

a. Inspection Scope

This area was inspected to: (1) ensure the gaseous and liquid effluent processing

systems are maintained so radiological discharges are properly mitigated, monitored,

and evaluated with respect to public exposure; (2) ensure abnormal radioactive gaseous

or liquid discharges and conditions, when effluent radiation monitors are out-of-service,

are controlled in accordance with the applicable regulatory requirements and licensee

procedures; (3) verify the licensee=s quality control program ensures the radioactive

effluent sampling and analysis requirements are satisfied so discharges of radioactive

materials are adequately quantified and evaluated; and (4) verify the adequacy of public

dose projections resulting from radioactive effluent discharges. The inspectors used the

requirements in 10 CFR Part 20; 10 CFR Part 50, Appendices A and I; 40 CFR Part 190;

the offsite dose calculation manual, and licensee procedures required by the technical

specifications as criteria for determining compliance. The inspectors interviewed

licensee personnel and reviewed and/or observed the following items:

  • Radiological effluent release reports since the previous inspection and reports

related to the effluent program issued since the previous inspection, if any

- 19 - Enclosure

  • Effluent program implementing procedures, including sampling, monitor setpoint

determinations and dose calculations

  • Equipment configuration and flow paths of selected gaseous and liquid discharge

system components, filtered ventilation system material condition, and significant

changes to their effluent release points, if any, and associated 10 CFR 50.59

reviews

  • Selected portions of the routine processing and discharge of radioactive gaseous

and liquid effluents (including sample collection and analysis)

  • Controls used to ensure representative sampling and appropriate compensatory

sampling

  • Results of the inter-laboratory comparison program
  • Effluent stack flow rates
  • Surveillance test results of technical specification-required ventilation effluent

discharge systems since the previous inspection

  • Significant changes in reported dose values, if any
  • A selection of radioactive liquid and gaseous waste discharge permits
  • Part 61 analyses and methods used to determine which isotopes are included in

the source term

  • Meteorological dispersion and deposition factors
  • Latest land use census
  • Records of abnormal gaseous or liquid tank discharges, if any
  • Groundwater monitoring results
  • Changes to the licensees written program for indentifying and controlling

contaminated spills/leaks to groundwater, if any

records, if any, and associated evaluations of the extent of the contamination and

the radiological source term

  • Offsite notifications, and reports of events associated with spills, leaks, or

groundwater monitoring results, if any

- 20 - Enclosure

  • Audits, self-assessments, reports, and corrective action documents related to

radioactive gaseous and liquid effluent treatment since the last inspection

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of the one required sample, as defined in

Inspection Procedure 71124.06-05.

b. Findings

No findings were identified.

2RS07 Radiological Environmental Monitoring Program (71124.07)

a. Inspection Scope

This area was inspected to: (1) ensure that the radiological environmental monitoring

program verifies the impact of radioactive effluent releases to the environment and

sufficiently validates the integrity of the radioactive gaseous and liquid effluent release

program; (2) verify that the radiological environmental monitoring program is

implemented consistent with the licensees technical specifications and/or offsite dose

calculation manual, and to validate that the radioactive effluent release program meets

the design objective contained in Appendix I to 10 CFR Part 50; and (3) ensure that the

radiological environmental monitoring program monitors non-effluent exposure

pathways, is based on sound principles and assumptions, and validates that doses to

members of the public are within the dose limits of 10 CFR Part 20 and

40 CFR Part 190, as applicable. The inspectors reviewed and/or observed the following

items:

  • Selected air sampling and thermoluminescence dosimeter monitoring stations
  • Collection and preparation of environmental samples
  • Operability, calibration, and maintenance of meteorological instruments
  • Selected events documented in the annual environmental monitoring report

which involved a missed sample, inoperable sampler, lost thermoluminescence

dosimeter, or anomalous measurement

  • Selected structures, systems, or components that may contain licensed material

and has a credible mechanism for licensed material to reach ground water

- 21 - Enclosure

as the result of changes to the land census or sampler station modifications since

the last inspection

  • Calibration and maintenance records for selected air samplers, composite water

samplers, and environmental sample radiation measurement instrumentation

  • Interlaboratory comparison program results
  • Audits, self-assessments, reports, and corrective action documents related to the

radiological environmental monitoring program since the last inspection

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of the one required sample as defined in

Inspection Procedure 71124.07-05.

b. Findings

No findings were identified.

2RS08 Radioactive Solid Waste Processing, and Radioactive Material Handling, Storage,

and Transportation (71124.08)

a. Inspection Scope

This area was inspected to verify the effectiveness of the licensee=s programs for

processing, handling, storage, and transportation of radioactive material. The inspectors

used the requirements of 10 CFR Parts 20, 61, and 71 and Department of

Transportation regulations contained in 49 CFR Parts 171-180 for determining

compliance. The inspectors interviewed licensee personnel and reviewed the following

items:

scope of the licensee=s audit program

  • Control of radioactive waste storage areas including container labeling/marking

and monitoring containers for deformation or signs of waste decomposition

  • Changes to the liquid and solid waste processing system configuration including

a review of waste processing equipment that is not operational or abandoned in

place

  • Radio-chemical sample analysis results for radioactive waste streams and use of

scaling factors and calculations to account for difficult-to-measure radionuclides

  • Processes for waste classification including use of scaling factors and

10 CFR Part 61 analysis

- 22 - Enclosure

  • Shipment packaging, surveying, labeling, marking, placarding, vehicle checking,

driver instructing, and preparation of the disposal manifest

  • Audits, self-assessments, reports, and corrective action reports radioactive solid

waste processing, and radioactive material handling, storage, and transportation

performed since the last inspection

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of the one required sample as defined in

Inspection Procedure 71124.08-05.

b. Findings

No findings were identified.

4. OTHER ACTIVITIES

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency

Preparedness, Public Radiation Safety, Occupational Radiation Safety, and

Physical Protection

4OA1 Performance Indicator Verification (71151)

.1 Data Submission Issue

a. Inspection Scope

The inspectors performed a review of the performance indicator data submitted by the

licensee for the first Quarter 2012 performance indicators for any obvious

inconsistencies prior to its public release in accordance with Inspection Manual

Chapter 0608, Performance Indicator Program.

This review was performed as part of the inspectors normal plant status activities and,

as such, did not constitute a separate inspection sample.

b. Findings

No findings were identified.

.2 Reactor Coolant System Specific Activity (BI01)

a. Inspection Scope

The inspectors sampled licensee submittals for the reactor coolant system specific

activity performance indicator for the period from the second quarter 2012 through the

first quarter 2012. To determine the accuracy of the performance indicator data reported

during those periods, the inspectors used definitions and guidance contained in NEI

Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6.

- 23 - Enclosure

The inspectors reviewed the licensees reactor coolant system chemistry samples,

technical specification requirements, issue reports, event reports, and NRC integrated

inspection reports for the period of April 1, 2011, through March 30, 2012, to validate the

accuracy of the submittals. The inspectors also reviewed the licensees issue report

database to determine if any problems had been identified with the performance

indicator data collected or transmitted for this indicator and none were identified.

These activities constitute completion of one reactor coolant system specific activity

sample as defined in Inspection Procedure 71151-05.

b. Findings

No findings were identified.

.3 Reactor Coolant System Leakage (BI02)

a. Inspection Scope

The inspectors sampled licensee submittals for the reactor coolant system leakage

performance indicator for the period from the second quarter 2011 through the first

quarter 2012. To determine the accuracy of the performance indicator data reported

during those periods, the inspectors used definitions and guidance contained in NEI

Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6.

The inspectors reviewed the licensees operator logs; reactor coolant system leakage

tracking data, issue reports, event reports, and NRC integrated inspection reports for the

period of April 1, 2011, through March 31, 2012, to validate the accuracy of the

submittals. The inspectors also reviewed the licensees issue report database to

determine if any problems had been identified with the performance indicator data

collected or transmitted for this indicator and none were identified. Specific documents

reviewed are described in the attachment to this report.

These activities constitute completion of one reactor coolant system leakage sample as

defined in Inspection Procedure 71151-05.

b. Findings

No findings were identified.

4OA2 Problem Identification and Resolution (71152)

.1 Routine Review of Identification and Resolution of Problems

a. Inspection Scope

As part of the various baseline inspection procedures discussed in previous sections of

this report, the inspectors routinely reviewed issues during baseline inspection activities

and plant status reviews to verify that they were being entered into the licensees

corrective action program at an appropriate threshold, that adequate attention was being

given to timely corrective actions, and that adverse trends were identified and

addressed. The inspectors reviewed attributes that included the complete and accurate

- 24 - Enclosure

identification of the problem; the timely correction, commensurate with the safety

significance; the evaluation and disposition of performance issues, generic implications,

common causes, contributing factors, root causes, extent of condition reviews, and

previous occurrences reviews; and the classification, prioritization, focus, and timeliness

of corrective actions. Minor issues entered into the licensees corrective action program

because of the inspectors observations are included in the attached list of documents

reviewed.

These routine reviews for the identification and resolution of problems did not constitute

any additional inspection samples. Instead, by procedure, they were considered an

integral part of the inspections performed during the quarter and documented in

Section 1 of this report.

b. Findings

No findings were identified.

.2 Daily Corrective Action Program Reviews

a. Inspection Scope

In order to assist with the identification of repetitive equipment failures and specific

human performance issues for follow-up, the inspectors performed a daily screening of

items entered into the licensees corrective action program. The inspectors

accomplished this through review of the stations daily corrective action documents.

The inspectors performed these daily reviews as part of their daily plant status

monitoring activities and, as such, did not constitute any separate inspection samples.

b. Findings

No findings were identified.

.3 Selected Issue Follow-up Inspection

a. Inspection Scope

The inspectors reviewed the causes and corrective actions for failure of containment

penetration assembly 274 electrical module A. This resulted in the loss of the

pressurizer backup group 1 heaters on March 18, 2012. The inspectors reviewed the

vendor hardware failure analysis report stating that a high resistance connection

developed in the butt splice inside the epoxy seal. The inspectors reviewed Wolf

Creeks apparent cause and extent of condition corrective actions and found that Wolf

Creek has visually inspected other similar penetrations. Wolf Creek also has corrective

actions perform thermography while penetrations are energized in order to detect failure

at an earlier stage. The inspectors compared Wolf Creeks evaluation with guidance

from the EPRI on containment building electrical penetration modules and did not find

any missing maintenance activities that may have prevented the loss of the pressurizer

backup group 1 heaters. Most degradation related to aging of the rubber seals in

- 25 - Enclosure

contact with the inner and outer surfaces of containment and not the electrical

conductors.

These activities constitute completion of one in-depth problem identification and

resolution sample as defined in Inspection Procedure 71152-05.

b. Findings

No findings were identified.

4OA3 Followup of Events and Notices of Enforcement Discretion (71153)

(Closed) Licensee Event Report 05000482/2012003-00, Train B ECCS Inoperable Due

to Damaged Watertight Containment Spray Pump Door Seal

On April 17, 2012, at 2:53 p.m., the watertight door seal for the train B containment spray

pump room was determined to be nonfunctional and the equipment supported by the

door was inoperable. The equipment supported by the door is the train B residual heat

removal pump and the train B containment spray pump. The door was repaired on

April 18, 2012, at 2:48 p.m. The watertight seal was replaced, welding was performed

on the knife-edge of the door and the door lugs were tightened. The apparent cause of

this condition was a less than adequate preventive maintenance to identify potentially

deficient door seals. This event is reportable under 10 CFR 50.73(a)(2)(i)(B) as an

operation or condition prohibited by Technical Specifications 3.5.2, 3.5.3, 3.6.6, and

Limiting Condition of Operation (LCO) 3.0.4. This condition is also reportable pursuant

10 CFR 50.73(a)(2)(v) as an event or condition that could have prevented the fulfillment

of a safety function because the opposite train was out of service several times while the

seal was degraded.

At the time of this licensee event report issued on June 18, 2012, the inspectors had

already inspected this event under baseline inspection procedure 71111.06. The results

of that inspection can be found in section 1R06 of this report.

These activities constitute completion of one event follow-up sample as defined in

Inspection Procedure 71151-05.

b. Findings

No findings were identified.

4OA5 Other Activities

Assessment of Corrective Action to Address Substantive Crosscutting Issues P.1.a,

P.1.c, and P.1.d

a. Inspection Scope

Wolf Creeks letter dated May 7, 2012, informed the NRC of its readiness for inspection

of substantive crosscutting issues P.1.a(problem identification), P.1.c(evaluation), and

- 26 - Enclosure

P.1.d(corrective action). From June 18 to 21, 2012, the inspectors gathered information

to inform managements decision in the mid-2012 performance assessment.

Consideration of possible closure of these substantive crosscutting issues will be an

NRC decision using information from this inspection, guidance in Inspection Manual

Chapter 0305, and the information discussed at a June 25, 2012, public meeting. The

inspectors reviewed whether the substantive crosscutting issues were entered into the

corrective action program (CAP), the causes identified, the corrective actions identified

to address those causes, the measures of effectiveness used by the licensee to monitor

improvement, and actual data for those effectiveness reviews.

This inspection activity constituted one sample of semi-annual trend review under

inspection procedure 1152-05.

b. Findings and Assessment

No findings were identified.

P.1.a entry into the CAP

Wolf Creek addressed all P.1 substantive crosscutting issues in two main condition

reports. Condition report 23032 was a root cause evaluation completed for a second

time in September 2010. Condition report 23032 was written in response to the problem

identification and resolution and human performance substantive crosscutting issues

that led the site to Column III of the NRCs action matrix. Wolf Creek identified 63

corrective actions that were to correct the problem identification and resolution problems.

Condition report 34455 was also a root cause in response to the 2010 end of cycle

assessment letter from the NRC. Condition report 34455 identified 27 corrective actions.

The inspectors concluded that the licensee appropriately entered this issue into the

CAP.

P.1.a Causes

Root and apparent cause evaluations were self-critical and they found a lack of

management involvement and oversight in the corrective action program over the last

3 years. These were the same causes identified for White performance indicators that

the 95002 team examined under condition report 23032. Condition report 23032 had a

second root cause that the station was over-confident in using the work controls process

to manage critical equipment problems. Root cause 34455 had a similar root cause of

leadership not aligning station behaviors for timely problem identification and resolution.

Root cause 34455 had a contributing cause that the station had inadequate training on

the design and licensing basis which is inhibiting effective problem evaluation. Further,

the root cause found that there was no regular training for certain personnel on the

design basis or its controls. The inspectors concluded that the licensee effectively

identified the causes for this substantive crosscutting issue.

P.1.a Corrective actions

The inspectors sampled corrective actions. The previous large change in the corrective

action program was to create the single point of entry for all issues into the CAP. This

- 27 - Enclosure

eliminated the previous practice of writing a work order for a problem, and only allowed

writing a condition report for each problem. While either method would work, the new

method added working level and management level scrutiny to each condition report.

The number of condition reports written increased since this change, often with multiple

condition reports on the same problem. This was implemented in January 2011, and

was responsive to 23032 root cause number two.

The inspectors observed that an important programmatic change to the Wolf Creek

corrective action software was implemented on April 26, 2012. Although it does not

appear to be directly linked to root cause 23032, a new department was formed which

added more oversight to operability determinations and work control, which was

responsive the root causes. Changes were made to track and evaluate degraded or

nonconforming conditions with a new department named operations work control. The

inspectors observed that the more recent immediate operability evaluations more closely

tie the equipment requirements to the observed problems to confirm or refute operability

or functionality (P.1.c). Also, the new changes track each degraded condition, and

prevent equipment from being returned to full service without a review of all corrective

actions by a senior reactor operator. The inspectors concluded that the added problem

evaluation scrutiny was consistent with the identified causes. Although many methods

of finding, evaluating, and fixing problems can work across the power reactor industry,

Wolf Creek chose to make CAP changes while instituting new guidance on the

accountability of the CAP. Based on a sampling review, the inspectors concluded that

the corrective actions were appropriate to address the identified causes.

P.1.a Corrective Action Effectiveness Measures

Wolf Creek internal metrics consisted of monitoring and trending the condition report

initiation rate overall by the site and department. Identification of the issues by the NRC

or other organizations, rather than by licensee personnel, negatively impact the metric.

Condition report initiation rate metrics showed a steady increase with most departments

having a high self identification rates in Green with the exception of three in the Red due

to NRC and external organization identification. The inspectors concluded that the

licensee had developed reasonable effectiveness measures, and that those

effectiveness measures demonstrated an improving trend for the station, but that the red

indicators reflected a continuation of a long standing trend in those areas.

P.1.a Results

The inspectors observed a low threshold for problems and condition reports. Personnel

interviewed indicated no hesitation to initiate condition reports. The inspectors observed

several issues had two or more condition reports for the same problem. Some problems

were consolidated to one condition report while others were not. More than one person

or work group may write a condition report for the same problem. Condition report

problem statements for those condition reports were not always reconciled to ensure

that all aspects would be corrected. This was consistent with the observations of the

biennial problem identification and resolution inspection documented in Inspection

Report 2012007.

P.1.c Entry into the CAP

- 28 - Enclosure

Wolf Creek addressed all P.1 substantive crosscutting issues in two main condition

reports and one condition report from 2008. Condition report 23032 was a root cause

evaluation completed for a second time in September 2010. Condition report 23032 was

in response to the problem identification and resolution and human performance

substantive crosscutting issues that led the site to being placed in Column III of the

NRCs action matrix. Wolf Creek identified 63 corrective actions that were to correct the

problem identification and resolution problems. Condition report 34455 also

documented a root cause analysis in response to the 2010 end of cycle assessment

letter from the NRC. Condition report 34455 identified 27 corrective actions. In the past,

Wolf Creek also took action under condition report 2008-8810 for the P.1.csubstantive

crosscutting issue. The causes for 2008-8810 were nearly identical to the more recent

root causes. The inspectors concluded that the licensee appropriately entered this issue

into the CAP.

P.1.c Causes

Root and apparent causes have been self-critical and they found a lack of management

involvement and oversight in the corrective action program over the last 3 years. These

were the same causes identified for White performance indicators that the 95002 team

examined under condition report 23032. Root cause 34455 has a similar root cause of

leadership not aligning station behaviors for timely problem identification and resolution.

Root Cause 34455 was written in March 2011 in response to the NRCs 2010

Assessment Letter, with the cause evaluation not completed until June 30, 2011. Root

cause 34455 had a contributing cause of the station having poor training on the design

and licensing basis which is inhibiting effective problem evaluation. A contributing cause

was the over-reliance on the work control process to getting problems fixed. Wolf Creek

has repeatedly found that less than timely evaluations have contributed to delays in

corrective actions for substantive cross cutting issues. The inspectors concluded that

the licensee effectively identified the causes for this substantive crosscutting issue.

P.1.c Corrective Actions

The inspectors sampled corrective actions. The previous large change in the corrective

action program was to create the single point of entry for all issues into the CAP. This

eliminated the previous practice of writing a work order for a problem, and only allowed

writing a condition report for each problem. While either method would work, the new

method added working level and management level scrutiny to each condition report.

The licensee recently implemented an important programmatic change involving

changes to the corrective action program software. Although it does not appear to be

directly linked to root cause 23032, a new department was formed which adds more

oversight to operability determinations and work control, which is responsive the root

causes. Changes were made to track and evaluate degraded or non-conforming

conditions with a new department named operations work control. The inspectors

observed that the more recent immediate operability evaluations more closely tie the

equipment requirements to the observed problems to confirm or refute operability or

functionality (P.1.c). Also, the new changes track each degraded condition and

equipment cannot be returned to full service without review of all corrective actions by a

senior reactor operator (P.1.d). The inspectors found the added problem evaluation

- 29 - Enclosure

scrutiny is consistent with the causes. Although many methods of finding, evaluating,

and fixing problems can work across the power reactor industry, Wolf Creek chose to

make CAP changes while instituting new guidance on the accountability of the CAP.

Most other corrective actions centered on recurring training for cause evaluators and

procedure changes to corrective action procedures, both directed at increasing the

quality of condition report causal evaluations.

P.1.c Corrective Action Effectiveness Measures.

The licensee developed evaluation quality internal performance indications, including the

results from corrective action review board and other challenge boards. The results of

these metrics were trending in a positive direction. These quality metrics and oversight

boards have undergone many changes in the last two years. The inspectors observed

that the trends reflect the refueling and forced outages, which typically cause an

increase in the number of evaluations needed. The operability evaluation metric up to

May showed a declining trend in quality over the last 6 months, though inspectors noted

that Wolf Creek did not find any evaluations that failed to demonstrate operability. Root

and apparent cause evaluation completion timeliness goals showed an improving trend

since October 2011, but are still Red and do not show average completion times that are

close to procedural limits. The inspectors concluded that the licensee had developed

reasonable effectiveness measures, although those effectiveness measures failed to

demonstrate sustained improvement.

P.1.c Results

Creating a single point of entry into the CAP was a significant change. The changes to

improve tracking of degraded or non-conforming conditions added some priority to fixing

problems, but giving priority to these types of items is still not a formal process

requirement. Corrective actions are still largely prioritized in the work control process.

Most corrective actions have focused on improving condition report evaluation

timeliness, providing evaluation methodology training (why tree, hazard-barrier-target,

etc.), and improving coding and trending of causes.

The inspectors interviewed department corrective action coordinators and found that

they had an active role in trending recurring problems in each department. The

inspectors saw this as a positive change but not directly related to evaluation quality.

Training on the plant design bases was positive and provided information on the overall

regulatory framework, but did not include specific requirements for the trainees systems

or engineering discipline. The inspectors saw improvement in the rejection of the root

cause by the corrective action review board for the January 13, 2012, loss of offsite

power, although not all rejections were captured by the stations metric.

The inspectors reviewed Wolf Creeks comprehensive event safety-significance

evaluation which examined all the problems revealed during the January 13, 2012, loss

of offsite power. Problem evaluation was stated as a contributing cause in that

self-assessment. Corrective actions were deferred to an apparent cause evaluation

stemming from a quality assurance audit that found the corrective action program

marginally effective. Corrective actions to that quality assurance assessment continued

the trend of changes to cause method training and CAP procedure changes. With

- 30 - Enclosure

design basis training being a self-identified weakness, inspectors observed that the

number and high-level content of those training courses will challenge the adequacy of

equipment specific problems, such as the leak seal repair in this report. The inspectors

concluded that progress was being made toward implementing the corrective actions for

this substantive cross-cutting issue, but that sustained improvement in the quality and

timeliness of evaluations had not been demonstrated.

P.1.d Entry into the CAP

Wolf Creek addressed all P.1 substantive crosscutting issues in two main condition

reports. Condition report 23032 was a root cause evaluation completed for a second

time in September 2010. Condition report 23032 was in response to the problem

identification and resolution and human performance substantive crosscutting issues

that led the site to Column III of the NRCs action matrix. Wolf Creek identified 63

corrective actions that were to correct the problem identification and resolution problems.

Condition report 34455 was also a root cause in response to the 2010 end of cycle

assessment letter from the NRC. Condition report 34455 identified 27 corrective actions.

The inspectors concluded that the licensee appropriately entered this issue into the

CAP.

P.1.d Causes

Root and apparent cause evaluations for this substantive cross-cutting issue were self-

critical, and they documented a lack of management involvement and oversight in the

corrective action program over the last 3 years. These are the same causes the 95002

team examined under condition report 23032. Root cause 34455 had a similar root

cause of leadership not aligning station behaviors for timely problem identification and

resolution. Root cause 34455 had a contributing cause of the station having inadequate

training on the design and licensing basis which was inhibiting effective problem

evaluation. These causes are the same as those for the P.1.a and P.1.csubstantive

cross-cutting issues. The previous large change in the corrective action program was to

create the single point of entry for all issues into the CAP. This eliminated the previous

practice of writing a work order for a problem, and only allowed writing a condition report

for each problem. While either method would work, the new method added working

level and management level scrutiny to each condition report. The licensee recently

implemented an important programmatic change involving changes to the corrective

action program software. Although it does not appear to be directly linked to root cause

23032, a new department was formed which adds more oversight to operability

determinations and work control, which is responsive the root causes Changes were

made to track and evaluate degraded or non-conforming conditions with a new

department named operations work control. The inspectors observed that the more

recent immediate operability evaluations were more closely tied the equipment

requirements to the observed problems in order to be able to confirm or refute operability

or functionality. Also, the new changes track each degraded condition, and required that

equipment cannot be returned to full qualification without review of all corrective actions

by a senior reactor operator. The inspectors concluded that the increased problem

evaluation scrutiny was consistent with the causes. Although many methods of finding,

evaluating, and fixing problems can work across the power reactor industry, Wolf Creek

chose to make CAP changes while instituting new guidance on the accountability of the

- 31 - Enclosure

CAP. The inspectors concluded that the licensee effectively identified the causes for this

substantive crosscutting issue.

P.1.d Corrective Actions

The inspectors reviewed selected corrective actions that were most responsive to the

root causes. Condition report 23032, action 2-9, instituted on August 31, 2011, required

the corrective actions review board review each issue coded as being a corrective action

to prevent recurrence within 30 days of its closure. Separate from the root causes, the

inspectors found other condition reports responding to NRC violations on annunciator

power supplies, emergency diesel loading, operability evaluations, and maintenance rule

stating that there was a need for continuing engineering training on standards for each of

those issues. The inspectors reviewed training lesson plans for change package

continuing training [modifications], Regulatory, Current Licensing Basis, And Design

Basis, and operability evaluation training for engineers and licensed operators. The

inspectors observed that the training was conducted every 60 days. Wolf Creek has

instituted corrective action backlog measurement indicators as a corrective action. The

inspectors noted that the act of trending is not a corrective action. Those backlogs

remain high, but have made some progress since the forced outage earlier this year.

Engineering also had a significant backlog of over 5500 work orders in May 2012. The

corrective action backlog initiative plan required regular meetings for departments to

drive a reduction in their backlog, but no other specific actions were developed, such as

addressing actions by priorities. The inspectors also noted that there were a significant

number of open actions to correct NRC violations, especially for scoping of maintenance

rule functions. Based on a sampling review, the inspectors concluded that the

corrective actions to address this substantive cross-cutting aspect were partially

appropriate to address the identified causes, but specific actions to ensure that CAP

corrective actions were timely and effective were lacking.

P.1.d Corrective Action Effectiveness Measures

Wolf Creeks effectiveness review for root cause condition report 23032 concluded that

there was not sustained improvement in ensuring that corrective actions were timely and

effective due to not meeting internal station metrics set for maintenance backlogs,

repetitive maintenance rule functional failures, and two other failed effectiveness follow-

ups. The interim effectiveness follow-up for root cause condition report 34455 was met

with the exception of one internal performance indicator for too great a ratio of NRC

identified to licensee identified findings. The inspectors observed that the identification

credit is an NRC function and affects the indicator, which may not be insightful. The

conclusion of condition report 34455 interim effectiveness review stated that additional

time was needed to increase the internal self-identification metrics and that more time

was needed. This effectiveness review also gave credit for future expected

improvement in the equipment performance index, a licensee metric, and which was

Yellow at the time of the inspection. The final effectiveness follow-up was scheduled to

be completed by December 20, 2012. The non-cited violation closure effectiveness

performance indicator was Red in January, February, and March 2012. Wolf Creek has

written two condition reports on the non-cited violation effectiveness performance

indicator and the need to return it to Green and are due to have formulated corrective

actions by August 9, 2012. The inspectors concluded that the licensee had developed

- 32 - Enclosure

reasonable effectiveness measures, although those effectiveness measures failed to

demonstrate sustained improvement.

P.1.d Results

The inspectors sampled input data and observed that Wolf Creek had self-critical

internal performance measures because those measurement methods and inputs were

found to reflect NRC identified and licensee-identified issues. The internal metrics for

trends in closure of condition reports, corrective action age, and the maintenance

backlog show recent positive improvement. The condition report 23032 measures of

effectiveness stated that the root cause actions will be effective when the equipment

reliability index and performance index reflect sustained improvement. The inspectors

reviewed the equipment reliability index and found that it is a culmination of several sub

indicators, which was Red until April 2012 when it became Yellow. One important

indicator the inspectors reviewed was the critical equipment failure indicator. The

inspectors noted that this indicator went from White to Red to White over the last year.

The inspectors observed that there was not sustained improvement in these internal

metrics.

The inspectors found a significant challenge in the number of open corrective actions in

response to NRC violations and findings. The inspectors reviewed effectiveness

followup evaluations for findings and violations in NRC inspection reports, and found

these effectiveness follow-ups to be sufficiently untimely that they may not provide an

independent check prior to recurrence or prevent unnecessary corrective action delay.

With a large backlog and many long term actions, effectiveness follow-ups continue to

wait for final corrective action completion because the licensee had no process to

perform interim effectiveness reviews when long-term actions were assigned. For

example, the inspectors reviewed an open corrective action to install heat tracing for

boric acid piping. The modification was complete, but relief valves have not been

installed and Wolf Creek was having to rely on a control room annunciator to have

operators respond prior to over-pressurization of piping. No time limit was given to the

annunciator response. The inspectors calculated the operators time limit to respond by

using the heat trace kilowatt rating and the heat capacity of the piping and water. The

inspectors found that operators had a reasonable amount of time, but Wolf Creek

initiated condition report 54278 to add a time constraint. Despite this corrective action

being over 3 years old and having three effectiveness follow-up extensions, corrective

action was not complete at the time of the inspection because the relief valves had not

been procured.

The inspectors also reviewed two issues related to NRC-identified problems with

emergency diesel generator testing. The inspectors found that the issue occurred a

second time due to inadequate corrective actions from a previous finding. The issue

was work in progress and thus was considered to be a minor issue within the inspection

program. Also, open corrective actions were inappropriately categorized as

enhancements to fix the post-maintenance testing deficiency. Wolf Creek subsequently

wrote action 49551-02-01 to make the necessary changes. The inspectors concluded

that progress was being made toward implementing the corrective actions for this

substantive cross-cutting issue, but that sustained improvement in the quality and

timeliness of evaluations had not been demonstrated.

- 33 - Enclosure

Overall Observations and Conclusions

Wolf Creek showed improvement in all three substantive cross-cutting areas by its

internal effectiveness measures and by a reduced number of NRC findings with those

crosscutting attributes. Wolf Creek has instituted many internal performance measures

as corrective actions. Every station has a policy or overarching safety guidance

document. Wolf Creek has made changes to that policy and instituted new ones for a

healthy safety culture. In addition to the stations policy, each department has

developed its own policy. Wolf Creek made changes to its accountability of personnel

for problem identification and resolution and other aspects of safety culture. This

includes changes to Wolf Creeks enforcement of these policies. The inspectors

observed that previous efforts to reinforce theses practices and organizational values

have not been successful. The inspectors interviewed selected personnel about the

safety culture changes. All staff interviewed welcomed changes to fix problems

promptly, but their feedback was mixed as to the effectiveness of changes such as

procedures and training. Nearly all interviewees expressed concern about their work

load and stations ability to correct problems.

4OA6 Meetings, Including Exit

Exit Meeting Summary

On April 26, 2012, the inspectors presented the results of the radiation safety inspection to

Mr. M. Sunseri, President and Chief Executive Officer, and other members of the licensee staff.

The licensee acknowledged the issues presented. The inspectors asked the licensee whether

any materials examined during the inspection should be considered proprietary. No proprietary

information was identified.

On July 18, 2012, the inspectors presented the inspection results to Mr. Richard Clemens, Vice

President of Strategic Projects, and other members of the licensee staff. The licensee

acknowledged the issues presented. The inspector asked the licensee whether any materials

examined during the inspection should be considered proprietary. All proprietary information

was returned or destroyed.

4OA7 Licensee-Identified Violations

The following violation of very low safety significance (Green) was identified by the licensee and

is a violation of NRC requirements which meets the criteria of the NRC Enforcement Policy for

being dispositioned as a non-cited violation.

.1 On January 31, 2012, Wolf Creek identified that inservice inspection for the second

10-year period were missed for two valves. Valves BB8379A and BB8379B are

chemical and volume control system alternate charging check valves to reactor coolant

system loop four. Both are ASME Code Class 1 valves. In 1987, valve BB8379B had a

leak at the body-to-bonnet joint and its studs were re-torqued. The valve continued to

leak a small amount. Subsequently, valves BB8379A and BB8379B each had a seal

cap, or leakage control device, installed on December 9, and 28, 1987, respectively.

- 34 - Enclosure

Title 10 CFR 50.55a(g)(4) requires licensees to follow the pressure test requirements of

the ASME Code Section XI. ASME Code,Section XI, IWA-5240, requires visual

examinations as part of system pressure tests. ASME Code Section XI, IWA-5242,

1998 Edition through 2000 addenda, requires pressure retaining bolted connections for

VT-2 visual examinations in borated water systems. Contrary to the above, from

September 3, 1995, to the present, Wolf Creek did not perform a visual inspection of the

valve body-to-bonnet studs. This finding was more than minor because it impacted the

Initiating Events Cornerstone and its attribute of equipment performance. Specifically, it

affected the objective to limit the likelihood of those events that upset plant stability and

challenge critical safety functions during shutdown as well as power operations. Using

Inspection Manual Chapter 0609, Appendix A ,The Significance Determination Process

(SDP) for Findings At-Power, this finding was determined to be of very low safety

significance because an evaluation was able to demonstrate structural integrity.

Specifically, stud stress was not sufficiently close to the yield stress to cause a loss of

integrity. Therefore, the finding does not contribute to both the likelihood of a reactor trip

and the likelihood that mitigation equipment will not be available. The licensee has

entered this issue into their corrective action program as condition reports 48493 and

48494. Wolf Creek planned to remove the seal caps and perform the inspection in the

next refueling outage.

- 35 - Enclosure

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

T. Baban, Manager, Systems Engineering

P. Bedgood, Manager, Radiation Protection

J. Broschak, Vice President, Engineering

S. Carpenter, Technician, Instruments and Controls

R. Clemons, Vice President, Strategic Projects

D. Dees, Superintendant, Operations

T. East, Superintendent, Emergency Planning

R. Evenson, Requalification Program Supervisor

R. Flannigan, Manager, Nuclear Engineering

K. Fredrickson, Engineer, Licensing

D. Gibson, Technician, Radiation Protection

R. Hammond, Supervisor, Regulatory Support

J. Harris, System Engineer

S. Henry, Operations Manager

R. Hobby, Licensing Engineer

S. Hossain, Engineer, System Engineering

T. Jensen, Manager, Chemistry

T. Just, Senior Technician, Chemistry

J. Keim, Support Engineering Supervisor

S. Koenig, Manager, Corrective Actions

M. McMullen, Technician, Engineering

C. Medenciy, Supervisor, Radiation Protection

W. Muilenburg, Licensing Engineer

M. McMullen, Design Engineer, Engineering

K. Miller, Technician Level III, Instruments and Controls

R. Murray, Simulator Supervisor

E. Ray, Manager, Training

L. Ratzlaff, Manager, Maintenance

T. Rice, Manager, Environmental Management

L. Rockers, Licensing Engineer

R. Ruman, Manager, Quality

G. Sen, Regulatory Affairs Manager

D. Scrogum, Systems Engineer, Engineering

R. Smith, Plant Manager

L. Solorio, Senior Engineer

M. Sunseri, President and Chief Executive Officer

J. Truelove, Supervisor, Chemistry

J. Weeks, System Engineer

M. Westman, Assistant to Site Vice President

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

A-1 Attachment

Opened and Closed

05000482/2012003-01 NCV Unacceptable Leakage Through Safety Related Watertight Door

During Loss of Offsite Power (Section 1R06)05000482/2012003-02 NCV Incorrect Leak Seal Injection Port Installation.

(Section 1R18)

Closed

05000482/2012-03-00 LER Train B ECCS Inoperable Due to Damaged Watertight

Containment Spray Pump Door Seal (Section 4OA3)

LIST OF DOCUMENTS REVIEWED

Section 1R01: Adverse Weather Protection

PROCEDURES

NUMBER TITLE REVISION

OFN SG-003 Natural Events 22

AI 14-006 Severe Weather 12

OFN AF-025 Unit Limitations 36

DRAWINGS

A-1320 Fuel Building Floor Plan 2047-6 and Roof 0

MISCELLANEOUS

OpESS 2012/01 Operating Experience Smart Sample High Wind Generated 0

Missile hazards

CONDITION REPORTS

51552 51562 46940

Section 1R04: Equipment Alignment

PROCEDURES

NUMBER TITLE REVISION

SYS GK-200 Inoperable Class IE A/C Unit 24

SYS EM-120 BIT Depressurization 2

A-2

DRAWINGS

NUMBER TITLE REVISION

M-12EM01 Piping & Instrumentation Diagram High Pressure Coolant 38

Injection System

M-12EM02 Piping & Instrumentation Diagram High Pressure Coolant 19

Injection System

CONDITION REPORTS

00053393 00053472 00053452 00053549 00053625

00053671 00053672 00053685 00053696 00053703

00053709 00053710 00053791 00053785 00053793

00053796 00053798 00048882

Section 1R05: Fire Protection

PROCEDURES

NUMBER TITLE REVISION

AP 10-106 Fire Preplans 12

AP 10-104 Breach Authorization 26

DRAWINGS

NUMBER TITLE REVISION

E-1F9905 Fire Hazard Analysis, Fire Area A-13 (Reference A-1803) 4

E-1F9905 Fire Hazard Analysis, Fire Area A-14 (Reference A-1804) 4

E-1F9905 Fire Hazard Analysis, Fire Area A-15 (Reference A-1804) 4

M-663-00017A Fire Protection Evaluations for Unique or Unbounded 3

Fire Barrier Configurations

Section 1R06: Flood Protection Measures

PROCEDURE

NUMBER TITLE REVISION

MPM XX-002 Water Tight Door Preventive Maintenance Activity 4

CONDITION REPORTS

A-3

51570 51622 52975 52794

Section 1R11: Licensed Operator Requalification Program

MISCELLANEOUS

NUMBER TITLE REVISION

LR4607005 Requal Simulator Exam Scenario 2

AP 21-001 Conduct of Operations 57

Section 1R12: Maintenance Effectiveness

PROCEDURES

NUMBER TITLE REVISION

WCOP-24 Operations EMG/OFN Setpoints 8

STN AE-007 Startup Main Feedwater Pump Operational Test 2 and 3

AP 16E-002 Post Maintenance Testing Development 10 and 11

MDI 06-01 Guidelines for Work Order Peer Review 6

EDI 23M-050 Engineering Desktop Instruction Monitoring Performance to 8

Criteria and Goals

STS ML-001 Monthly Surveillance Log 45

SB-01 Reactor Protection systems

CONDITION REPORTS

51655 51706 41997 53417 35413

35426 35532 35533 35535 35537

35539 35540 35541 35542 35544

35545 35546 35547 35548 35549

35550 35551 35552 35553 35554

35555 35558 35560 35614 35615

35617 35619 35620 35621 35622

35623 35624 35625 35626 35627

35628 35629 35882 36012 35013

36014 36038 36039 36040 36041

36042 36043 36044 36045 36057

A-4

36058 36060 36061 36062 36064

36065 36078 36079 36080 36081

36082 3608336084 36117 36118 36119

36134 36135 38108 40687 40753

46341 48955 49672 49738

WORK ORDER

11-346146-003

PERFORMANCE IMPROVEMENT REQUESTS

36518 36777 37048 37107 37439

37482 37615 38003 38023 38106

38162 38108 38369 38487 38488

38873 39349 39350 39351 39365

43639 49672 54110 54163 54164

45414

CALCULATIONS

NUMBER TITLE REVISION

AN-11-007 Startup Feedwater Pump (PAE02) Flow Rate Required to 0

Remove Decay Heat Following Reactor Shutdown

DRAWINGS

NUMBER TITLE REVISION

M-12AE01 Piping & Instrumentation Diagram Feedwater System 38

Section 1R13: Maintenance Risk Assessment and Emergent Work Controls

PROCEDURES

NUMBER TITLE REVISION

NK-022 Load Test 2

STS-MT-020 125 Volt DC Battery Inspection/Charger Operational Test 25B

CONDITION REPORTS

A-5

51421 51565

WORK ORDERS

06-281938-000 04-259540-000 04-259542-000 12-353322-000 12-353322-001

DRAWINGS

NUMBER TITLE REVISION

E-051-00058 Three phase SCR Controller Battery Charger Schematic WO7

WIP-M-761- SNUPPS Process Control Block Diagram+ 00

00075-W08-A-1

MISCELLANEOUS

NUMBER TITLE DATE

N/A On-Line Nuclear safety and Generation Risk Assessment May 30, 2012

Section 1R15: Operability Evaluations

DRAWINGS

NUMBER TITLE REVISION

M-724-00276 Swing Check Valve W04

OE BB12-004 BB8397A/B CVCS Alternate Charging to Loop 4 Check 1

Valve

MGM MOOP-08 Torquing Guidelines for Bolted Connections 13

RR-87-060 ASME Section XI Repair/Replacement Plan 0

RR-87-060 ASME Section XI Repair/Replacement Plan 1

PROCEDURES

NUMBER TITLE REVISION

EPP 06-002 Technical Support Center Operations 30A

EPP 06-013 Exposure Control and Personnel Protection 6

EMG E-0 Reactor Trip or Safety Injection 27

CALCULATIONS

NUMBER TITLE REVISION

AN 99-020 Control Room Habitability of a Postulated LOCA, based on a 2

Control Room Unfiltered Inleakage of 20.0 cfm

A-6

CALCULATIONS

NUMBER TITLE REVISION

GK-M-001 Safety Related Control Room Building HVAC Capabilities 2

During Accident Conditions (SGK04A/B and SGK05A/B)

GK-E-001 Electrical Equipment Heat Loads in ESF SWGR, DC SWBD, 2

& Battery Rooms

MISCELLANEOUS DOCUMENTS

NUMBER TITLE REVISION /

DATE

ITLS Report 24045 Liquid Penetrant Inspection of Submitted Machined August 7, 1978

Parts

Jessop Steel Company - Ultrasonic Inspection Report June 28, 1978

Operability Evaluation OE BB-12-004 00

Case N-616 Cases of ASME Boiler and Pressure Vessel Code May 7, 1999

SAP-12-58 Westinghouse LTR-SEE-III-12-81 April 14, 2012

128136 Westinghouse Drawing Revision - Material Changes September 28,

1993

CA2412 1st & 2nd Off Check Valve PMs December 26,

2008

OE BB12-004 BB8397A/B CVCS Alternate Charging to Loop 4 Check 00

Valve

CA4790 Write PMC Work Request December 26,

2008

CA4791 Revise AP 23F-001 December 26,

2008

CA4792 Update BID-CV-1 December 26,

2008

M-622.1 (Q) Design Specifcation for Packaged Air Conditioning Units 9

WORK REQUESTS

03611-87 00122-87

CONDITION REPORTS

00048493 00048494 00051530 003419 0052822

A-7

WORK ORERS

07-295490-000 08-309436-000 10-324925-000 10-327516-000 10-327516-001

10-324925-000 10-331280-000 10-327516-000 11-339107-001 11-339107-002

11-339107-000 12-351057-000 00-223094-011

Section 1R18: Plant Modifications

NUMBER TITLE REVISION /

DATE

BMV0037 Furmanite Adapter Installation Evaluation 00

MPM LR-001 Leak Sealant Injection 7

WCN-00-001 Reedy Engineering, Inc. No 00-216961-000 0

ECW-119 Furmanite The Solutions Group 0

DRAWINGS

NUMBER TITLE REVISION /

DATE

M-240-00072 Valve Assembly - 2 IN Diaphragm Y Type, Globe 1522 3

LB.C.S

1974 ASME Code, Article NC-3000

1986 ASME Code, NC-3229

1983 ASME Code, NC3232.2

Fig NC3329(g)-1 1986 Edition ASME Code

MPM LR-001 Leak Sealant Injection 7

Change Package Furnmanite Adapter Fitting and BMV0037 Furmanite Repair 00

013482

ECW-119 Pressure Seal Calculation Sheet 0

CONDITION REPORT

52992

WORK ORDERS

10-333183-002 10-333183-009 11-346576-002 11-346576-003 11-346576-006

11-346576-009 11-346576-010 11-346576-015 11-346576-017

A-8

Section 1R19: Postmaintenance Testing

PROCEDURES

NUMBER TITLE REVISION

MPE GK-003 Control Room and Class 1E A/C Units Preventive 3A

Maintenance Activity

MPE GK-004 GK Unit Preparation for Work 4

STS IC-500G Channel Calibration DT/TAVG Instrumentation Loop 4 22A

STS IC-204A Channel Operational Test of TAVG, dT and Pressurizer 17B

Pressure Protection Set Four

INC C-0026 7300 Lead/Lag Card (NLL0G01 Artwork Revisions 12) 2A

INC C-0016 7300 Summing AMP Card (NSA1 and NSA2) 10A

STS IC-502B Channel Calibration of 7300 Process Pressurizer Pressure 16

Instrumentation

STS IC-444 Channel Calibration NIS Power Range N-44 11B

WORK ORDERS

12-354805-003 11-348929-000 11-348929-002 11-348929-003 11-348929-004

11-348929-005 12-355385-001 12-355293-001 12-355293-004 12-355293-005

DRAWINGS

NUMBER TITLE REVISION

E-13GK13A Schematic Diagram Class IE Electrical Equipment A/C Unit 6

QCP-20-514 Eddy Current Examination Technique Sheet 5C

Eddy Current Calibration Summaries

WIP-M-761- Interconnecting wiring diagram cabinet 04 SNUPPS Nuclear 00

02102-004-A-1 Power Plant Controls

WIP-M-761- Interconnecting wiring diagram cabinet 04 SNUPPS Nuclear 00

02088-W08-A-1 Power Plant Controls

M-761-02084 Interconnecting wiring diagram cabinet 04 SNUPPS Nuclear W20

Power Plant Controls

A-9

Section 1R22: Surveillance Testing

PROCEDURES

NUMBER TITLE REVISION

ABHV0011 Solenoid Block Replacement

STS AB-205 Main Steam System Inservice Valve Test 29

6101-00007 CS Innovations LLC 2008 Confidential and Proprietary 2

J-105A-00013 MSFIS Information, Operation & Maintenance Manual W02

SY1503900 Standard Functional Description of System Medium W01

Operated Isolation Valves

Main and Reheat Steam System 18

STS EJ-100A RHR System Inservice Pump A Test 45

STS EN-100B Containment Spray Pump B Inservice Pump Test 26

TMP 11-013 ECCS Check Valve Leak Check 2

WCOP-02 Inservice Testing Program Third Ten-Year Interval 14

CALCULATIONS

NUMBER TITLE REVISION

AN 06-017 Steamline Break Core Response Analysis to Support 0

MSIV/MFIV Replacement Project (DCP #09952)

AN 06-018 Feedwater Line Break Analysis to Support the MSIV/MFIV 0

Replacement Project (DCP #09952)

AN-06-019 0

SGTR Stuck Open ARV Analysis to Support the MSIV/MFIV

Replacement Project (DCP #09952)

AN-06-020 Steam Generator Tube Rupture Overfill Analysis to Support 0

the MSIV/MFIV Replacement Project (DCP #09952)

EJ-100A Pump: PEJ01A: Group A

DRAWINGS

NUMBER TITLE REVISION

M-628-00140 MSIV System Medium Actuator Schematic W01

M630-00124 Standard Functional Description of System Medium W01

Operated Isolation Valves

CONDITION REPORTS

A-10

51396 51995

Section 4OA1: Performance Indicator Verification

PROCEDURES

NUMBER TITLE REVISION

STS BB-006 Reactor Coolant System Inventory Balance Using NPIS 9

Computer

AP 26A-007 NRC Performance Indicators 8

STS CH-025 Reactor Coolant Dose Equivalent Iodine Determination 5

MISCELLANEOUS DOCUMENTS

NUMBER TITLE REVISION

NEI 99-02 Regulatory Assessment Performance Indicator Guidelines 6

Section 4OA2: Identification and Resolution of Problems

MISCELLANEOUS DOCUMENTS

NUMBER TITLE REVISION /

DATE

12-1119-L-01 Final Report on Laboratory Evaluation of Failed Containment May 8, 2012

50754 Electrical Penetration Assembly ZNE274 Module A; Purchase

Order No. 758996/0Pressurizer Heater Cables Found Burnt

WM 12-0013 Notification of Readiness for Inspection of Human May 7, 2012

Performance and Problem Identification and Resolution

Safety Culture Themes for the Wolf Creek Generating Station

Wolf Creek Station-Wide Fundamental Behaviors Mar 19, 2012

Corrective Action Recovering Monitoring Metrics May 2012

Corrective Action Recovering Monitoring Metrics September

2011

Letter No. SL- Transmittal of Summary of Results for RELAP ESW June 19,

WC-2012-003 Waterhammer Analysis 2012

IIT 12-001 Comprehensive Event Safety Significance Assessment

P.1(c) WCNOC Activities Associated with Resolutions of NRC June 6, 2012

Cross-Cutting Aspect P.1(c)

P.1(a) WCNOC Activities Associated with Resolution of NRC Cross- June 6, 2012

Cutting Aspect P.1(a)

A-11

MISCELLANEOUS DOCUMENTS

NUMBER TITLE REVISION /

DATE

P.1(d) WCNOC Activities Associated with Resolution of NRC Cross- June 6, 2012

Cutting Aspect P.1(d)

Corrective Action Backlog Reduction Initiative May 2012

AI 28A-006 Apparent Cause Evaluation 2

CONDITION REPORTS

15367 23032 26691 34455 51952

48182 48642 50807 50754 50809

51207 51290 51303 51408 51464

51429 51698 51952 53137 54278

Section 4OA5: Other Activities

PROCEDURES

NUMBER TITLE REVISION

AP 28A-100 Condition Reports 16

ALR 00-037E CVCS HT Trace 8

SYS BG-206 Boric Acid System Operation 40

AI-22A-001 Operator Work Arounds/Operator Burdens/Control Room 10A

Deficiencies

AE-04-51 Provide feedwater and controls to the steam generator

(startup feedpump)

DRAWINGS

NUMBER TITLE REVISION

M-12BG05 Piping & Instrumentation Diagram Checmical & Volume 17

Control System

CALCULATION

NUMBER TITLE REVISION

BG-M-051 0

QUICK HIT DETAIL REPORT

A-12

1953

CONDITION REPORTS

20709 20717 21039 27909 29602

30995 31129 31746 32129 34730

34065 34455 36600 39846 39847

39848 39849 39850 39851 39852

40714 43454 45218 48234 49551

50052 52151-01 5222-01 52447-01 52613-01

52580 52851 53024 53793-01 53791-01

54238 54239 54240

MISCELLANEOUS DOCUMENTS

NUMBER TITLE REVISION /

DATE

Page 15 0f 31 Apparent Cause Evaluation Time SCCI P.1/c

AL 28A-100 Cause Evaluations April 24, 2012

SEL 2010-189 RIS 2005-20 Alignment Benchmark November 8

and 22, 2010

Change Package 013130 15

WC-NRC Component Design Bases Inspection NRC January 11,

Inspection Report 05000482/2010007 2011

BLSE 578 SNUPPS Project Diesel Generator Building Ventilation March 27,

File 7854 System Description 1974

BLSE-435 SNUPPS Project Heating, Ventilation, and Air Conditioning

File 7850 Design Criteria

Maintenance Rule Expert Panel Meeting Minutes April 19, 2012

EDI 23M-250 Engineering Desktop Instruction Monitoring Performance to 3

Criteria and Goals

K15-002 Audit 12-04-CAP Corrective Action Program May 21, 2012

WORK ORDERS

10-332371-009 10-332371-022 10-332371-038

PERFORMANCE IMPROVEMENT REQUESTS

A-13

49220 42496

A-14