ML060450209: Difference between revisions

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#REDIRECT [[IR 05000458/2005005]]
{{Adams
| number = ML060450209
| issue date = 02/13/2006
| title = IR 05000458-05-005; on 10/01/2005 - 12/31/2005; River Bend Station; Licensed Operator Requalification, Operator Performance During Nonroutine Plant Evolutions, Permanent Plant Modifications
| author name = Kennedy K
| author affiliation = NRC/RGN-IV/DRP/RPB-C
| addressee name = Hinnenkamp P
| addressee affiliation = Entergy Operations, Inc
| docket = 05000458
| license number = NPF-047
| contact person =
| document report number = IR-05-005
| document type = Inspection Report, Letter
| page count = 41
}}
See also: [[see also::IR 05000458/2005005]]
 
=Text=
{{#Wiki_filter:February 13, 2006Paul D. HinnenkampVice President - Operations
Entergy Operations, Inc.
River Bend Station
5485 US Highway 61N
St. Francisville, Louisiana 70775SUBJECT:RIVER BEND STATION - NRC INTEGRATED INSPECTIONREPORT 05000458/2005005Dear Mr. Hinnenkamp:
On December 31, 2005, the U.S. Nuclear Regulatory Commission (NRC) completed aninspection at your River Bend Station.  The enclosed integrated inspection report documentsthe inspection findings which were discussed with you and other members of your staff on
January 4, 2006.The inspection examined activities conducted under your license as they relate to safety andcompliance with the Commission's rules and regulations and with the conditions of your license.
The inspectors reviewed selected procedures and records, observed activities, and interviewed
personnel.Based on the results of this inspection, two NRC identified findings and one self-revealingfinding were evaluated under the risk significance determination process as having very low
safety significance (Green).  The NRC has also determined that violations are associated withthese findings.  However, because these violations were of very low safety significance and
were entered into your corrective action program, the NRC is treating these violations as
noncited violations, consistent with Section VI.A.1 of the NRC's Enforcement Policy.  If youcontest the violations or the significance of the violations, you should provide a response within30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear
Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, withcopies to the Regional Administrator, U.S. Nuclear Regulatory Commission, Region IV, 611
Ryan Plaza Drive, Suite 400, Arlington, Texas 76011-4005; the Director, Office of Enforcement,U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resi dentInspector at the River Bend Station facility.In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, itsenclosure, and your response (if any) will be available electronically for public inspection in theNRC Public Document Room or from the Publicly Available Records (PARS) com
ponent ofNRC's document system (ADAMS).  ADAMS is accessible from the NRC Website at
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Entergy Operations, Inc.-2-Should you have any questions concerning this inspection, we will be pleased to discuss themwith you.Sincerely,/RA/Kriss M. Kennedy, ChiefProject Branch C
Division of Reactor ProjectsDocket:  50-458License:  NPF-47Enclosures:NRC Inspection Report 05000458/2005005  w/Attachment:  Supplemental Informationcc w/enclosure:Senior Vice President and
  Chief Operating Officer
Entergy Operations, Inc.
P.O. Box 31995
Jackson, MS  39286-1995Vice President Operations Support
Entergy Operations, Inc.
P.O. Box 31995
Jackson, MS  39286-1995General ManagerPlant Operations
Entergy Operations, Inc.
River Bend Station
5485 US Highway 61N
St. Francisville, LA 
70775Director - Nuclear SafetyEntergy Operations, Inc.
River Bend Station
5485 US Highway 61N
St. Francisville, LA 
70775
Entergy Operations, Inc.-3-Wise, Carter, Child & Caraway
P.O. Box 651
Jackson, MS  39205Winston & Strawn LLP1700 K Street, N.W.
Washington, DC  20006-3817Manager - LicensingEntergy Operations, Inc.
River Bend Station
5485 US Highway 61N
St. Francisville, LA 
70775The Honorable Charles C. Foti, Jr.Attorney General
Department of Justice
State of Louisiana
P.O. Box 94005
Baton Rouge, LA  70804-9005H. Anne Plettinger
3456 Villa Rose DriveBaton Rouge, LA  70806Burt Babers, PresidentWest Feliciana Parish Police Jury
P.O. Box 1921
St. Francisville, LA 
70775Michael E. Henry, State Liaison OfficerDepartment of Environmental Quality
Permits Division
P.O. Box 4313
Baton Rouge, LA  70821-4313Brian AlmonPublic Utility Commission
William B. Travis Building
P.O. Box 13326
1701 North Congress Avenue
Austin, TX  78711-3326
Entergy Operations, Inc.-4-ChairpersonDenton Field Office
Chemical and Nuclear Preparedness
  and Protection Division
Office of Infrastructure Protection
Preparedness Directorate
Dept. of Homeland Security
800 North Loop 288
Federal Regional Center
Denton, TX  76201-3698
Entergy Operations, Inc.-5-Electronic distribution by RIV:Regional Administrator (BSM1)DRP Director (ATH)DRS Director (DDC)DRS Deputy Director (RJC1)Senior Resident Inspector (PJA)Branch Chief, DRP/C (KMK)Senior Project Engineer, DRP/C (WCW)Team Leader, DRP/TSS (RLN1)RITS Coordinator (KEG)DRS STA (DAP)J. Dixon-Herrity, OEDO RIV Coordinator (JLD)ROPreports
RBS Site Secretary (LGD)W. A. Maier, RSLO (WAM)SUNSI Review Completed:  _kmk_ADAMS:  Yes G  No            Initials: __kmk__    Publicly Available     
G  Non-Publicly Available     
G  Sensitive  Non-SensitiveR:\_REACTORS\_RB\2005\RB2005-05RP-PJA.wpdRIV:SRI:DRP/CRI:DRP/CC:DRS/OBC:DRS/EB1C:DRS/PSBPJAlterMOMillerATGodyJClarkMPS
hannon T - KMKennedy E - KMKennedy      /RA/      /RA/        /RA/2/    /062/    /062/    /062/    /062/    /06C:DRS/EB2C:DRP/CLJSmithKMKennedy  GDReplogle for      /RA/2/13/062/13/06OFFICIAL RECORD COPY T=Telephone          E=E-mail        F=Fax
Enclosure-1-U.S. NUCLEAR REGULATORY COMMISSIONREGION IVDocket:50-458License:NPF-47
Report:05000458/2005005
Licensee:Entergy Operations, Inc.
Facility:River Bend StationLocation:5485 U.S. Highway 61St. Francisville, LouisianaDates:October 1 through December 31, 2005
Inspectors:P. Alter, Senior Resident Inspector, Project Branch CM. Miller, Resident Inspector, Project Branch CJ. Keeton, Consultant, Region IV
P. Elkmann, Emergency Preparedness Inspector, Operations Branch
G. Johnston, Senior Operations Engineer, Operations Branch
L. Ricketson, Senior Health Physicist, Plant Support BranchApproved By:Kriss M. Kennedy, ChiefProject Branch C
Division of Reactor Projects
Enclosure-2-TABLE OF CONTENTSSUMMARY OF FINDINGS....................................................3REPORT DETAILS..........................................................5
REACTOR SAFETY.........................................................51R01Adverse Weather Protection
.......................................51R04Equipment Alignment
.............................................61R05Fire Protection
..................................................71R11Licensed Operator Requalification
...................................81R13Maintenance Risk Assessments and Emergent Work Control.............101R14Operator Performance During Non-routine Plant Evolutions..............111R15Operability Evaluations..........................................141R16Operator Work-Arounds.........................................151R17Permanent Plant Modifications....................................151R19Postmaintenance Testing........................................171R22Surveillance Testing............................................181R23Temporary Plant Modifications....................................191EP2Alert and Notification System Testing...............................191EP3Emergency Response Organization Augmentation.....................201EP5Correction of Emergency Preparedness Weaknesses and Deficiencies.....201EP6Drill Evaluation.................................................21RADIATION SAFETY.......................................................222OS2ALARA Planning and Controls.....................................22OTHER ACTIVITIES........................................................234OA1Performance Indicator Verification..................................234OA2Identification and Resolution of Problems............................234OA3Event Followup................................................264OA6Meetings, Including Exit..........................................27SUPPLEMENTAL INFORMATION............................................A-1
KEY POINTS OF CONTACT................................................A-1
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED...........................A-1LIST OF DOCUMENTS REVIEWED..........................................A-2
LIST OF ACRONYMS......................................................A-8
Enclosure-3-SUMMARY OF FINDINGSIR 05000458/2005005; 10/01/2005 - 12/31/2005; River Bend Station; Licensed OperatorRequalification, Operator Performance During Nonroutine Plant Evolutions, Permanent PlantModifications.The report covered a 3-month period of routine baseline inspections by resident inspectors andannounced baseline inspections by regional emergency planning, operations, and radiation
protection inspectors.  Three Green noncited violations were identified.  The significance of
most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual
Chapter 0609, "Significance Determination Process."  Findings for which the significance
determination process does not apply may be Green or be assigned a severity level after NRC
management review.  The NRC's program for overseeing the safe operation of commercialnuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 3,dated July 2000.A.NRC-Identified and Self-Revealing FindingsCornerstone:  Initiating Events*Green.  The NRC identified a noncited violation of Technical Specification 3.4.1.A for thelicensee's failure to shut down one reactor recirculation loop within 2 hours of
determining that jet pump loop flow mismatch was greater than 5 percent whileoperating at greater than 70 percent of rated core flow.  On October 31, 2005, theReactor Recirculation Flow Control Valve B hydraulic power unit tripped because of a
blown control power fuse, causing Flow Control Valve B to drift open.  Operators
throttled closed Flow Control Valve A to maintain reactor power at 100 percent, resulting
in a jet pump loop flow mismatch of approximately 8.2 percent.  The flow mismatch
existed for 4.5 hours.  The licensee entered this into their corrective action program as
Condition Report CR-RBS-2006-00274. The finding was more than minor because, if left uncorrected, it would become a moresignificant safety concern.  Matched recirculation loop flows is an assumption used in
the accident analysis for a loss of coolant accident resulting from a loop break.  A flow
mismatch could result in core response that is more severe than assumed in the
accident analysis.  The significance of this finding could not be evaluated using
MC 0609, "Significance Determination Process."  Based on management review, the
finding was determined to be of very low safety significance based on the short duration
of the flow mismatch, 4.5 hours, and the low likelihood of a loss of coolant accident
during that time.  The cause of this finding is related to the crosscutting element ofhuman performance in that operators failed to implement Technical Specification
requirements (Section 1R14).Cornerstone:  Mitigating Systems
*Green.  A self-revealing noncited violation of 10 CFR Part 50, Appendix B, Criterion
III,Design Control, was identified for the licensee's failure to address the worst case
conditions in the sizing calculation for the reactor core isolation cooling turbine exhaust
Enclosure-4-line vacuum breaker system as part of a plant modification to remove the internals of thereactor core isolation cooling turbine exhaust line check valve.  As a result, on
December 10, 2004, when the reactor core isolation cooling system was started andsubsequently shutdown on high reactor water level following a scram and loss of
feedwater, the turbine exhaust line filled with water from the suppression pool, causingthe operators to consider t
he system unavailable and complicating their response to theevent.  The licensee entered this finding into their corrective action program as CR-
RBS-2005-00724 and reinstalled the turbine exhaust line check valve internals in
February 2005. The finding was more than minor because it was associated with the Mitigating Systemscornerstone attribute of Design Control and affected the cornerstone objective to ensure
the availability and reliability of the reactor core isolation cooling system, a system thatresponds to initiating events (loss of feedwater and station blackout), to prevent
undesirable consequences.  Using Manual Chapter 0609, "Significance Determination
Process," Phase 1 Worksheet, the finding was determined to have very low safety
significance because it represented a design deficiency that did not result in a loss of
system function (Section 1R17).Cornerstone:  Emergency Preparedness
*Green.  The NRC identified a noncited violation of 10 CFR Part 50, Appendix E,Section IV. B., as a result of inadequate procedures for the implementation of an
emergency action level.  The criteria in Procedure EIP-2-001, "Classification of
Emergencies," Revision 12, for declaring an Alert emergency action level based on
primary coolant leak rate, relied solely on a computer generated leakrate report that
would not be valid under all conditions.  The licensee entered this finding into their
corrective action program as CR-RBS-2005-03078 and issued Standing Order 192, as
an interim corrective action, to provide additional criteria to determine whether a primary
coolant leak rate Alert emergency action level declaration was required.The finding is more than minor because it is associated with the EmergencyPreparedness Cornerstone attribute of procedural quality and affects the cornerstone
objective to ensure the licensee is capable of implementing adequate measures to
protect the health and safety of the public in the event of a radiological emergency.  The
inadequate procedure could result in a failure to declare an Alert emergency
classification when required.  Using Manual Chapter 0609, Appendix B, "Emergency
Preparedness Significance Determination Process," this finding was determined to be of
very low safety significance since it was a failure to comply with a regulatory
requirement associated with a risk-significant planning standard that did not result in the
loss or degradation of that risk-significant planning standard function (Section 1R11).B.Licensee-Identified Violations
None.
Enclosure-5-REPORT DETAILSSummary of Plant Status
  On October 1, 2005, reactor power was lowered to 70 percent to perform a rod sequenceexchange and insert two control rods for planned maintenance.  The reactor was returned to
100 percent power on October 2, 2005.  On October 21, 2005, reactor power was lowered to 63percent to perform power suppression testing for a leaking fuel bundle.  The reactor was
returned to 100 percent power on October 23, 2005.  On November 5, 2005, reactor power was
lowered to 90 percent to adjust the control rod pattern and the reactor was returned to 100
percent later that day.  On December 2, 2005, reactor power was lowered to 83 percent to
insert three control rods for planned maintenance.  The reactor was returned to 100 percent
power on December 3, 2005.  On December 9, 2005, reactor power was lowered to 58 percent
to perform a control rod pattern adjustment and conduct turbine valve testing.  The reactor was
returned to 100 percent power on December 11, 2005.  On December 17, 2005, reactor power
was lowered to 62 percent to perform power suppression testing for a leaking fuel bundle.  The
reactor was returned to 100 percent on December 19, 2005, and remained at 100 percent for
the remainder of the inspection period.1.REACTOR SAFETYCornerstones:  Initiating Events, Mitigating Systems, Barrier Integrity, EmergencyPreparedness1R01Adverse Weather Protection    b.Inspection ScopeCold Weather PreparationDuring the week of December 5, 2005, the inspectors reviewed the licensee'simplementation of Operations Section Procedure OSP-0043, "Freeze Protection andTemperature Maintenance," Revision 6, to protect mitigating systems from cold weatherconditions.  Specifically, the inspectors:  (1) verified that risk-significant structures,
systems, and components will remain functional when challenged by cold weatherconditions; (2) verified that cold weather features such as heat tracing and space
heaters are operable and monitored; and (3) verified that the cold weather proceduresattachments were being completed for changing temperatures as required by the
procedure.  The inspectors completed one inspection sample.      c.FindingsNo findings of significance were identified.
Enclosure-6-1R04Equipment Alignment  1.Partial System Walkdowns    a.Inspection Scope
    On October 25, 2005, the inspectors walked down residual heat removal Division II
while residual heat removal Division I was out of service for scheduled maintenance.
On October 26, 2005, the inspectors walked down the piping and valve lineup of the
condensate storage tank, including emergency core cooling system suction and testreturn valves.  In each case, the inspectors verified the correct valve and power
alignments by comparing positions of valves, switches, and electrical power breakers to
 
the system operating procedures (SOP) and piping and instrument drawings listedbelow and applicable sections of the Updated Safety Analysis Report (USAR).  The
inspectors completed two inspection samples.  *SOP-0031, "Residual Heat Removal System," Revision 46
*SOP-0008, "Condensate Storage, Makeup and Transfer," Revision 16
*Piping and Instrument PID 04-03A, "Condensate Storage, Makeup andTransfer," Revision 13    b.FindingsNo findings of significance were identified.  2.Complete System Walkdown    a.Inspection ScopeThe inspectors conducted a complete walkdown of the drywell and containment leakdetection system during the week of June 26, 2005, during a drywell closeout inspectionand continuing the week of November 20, 2005.  The methods of inspection included
field walkdown, in-office reviews, observation of system operation, and interviews ofcomputer engineering, operations, training, and emergency planning personnel.  The
inspectors verified:  (1) proper valve and control switch alignments, (2) computer
program algorithm, (3) power supply lineup, (4) associated support system st
atus, and(5) that alarms and indications in the main control room were as specified in the
following documents:*SOP-0033, "Drywell and Containment Leak Detection System," Revision 11*USAR Section 5.2.5.1.1, "Detection of Leakage within the Drywell"*Technical Specifications (TS) Section 3.4.5, "RCS Operational Leakage"The inspectors also verified electrical power requirements, labeling, hangers andsupport installation, and associated support systems status.  The walkdowns included
Enclosure-7-evaluation of system piping and supports to ensure (1) piping and pipe supports did notshow evidence of damage, (2) hangers were secure, and (3) component foundations
were not degraded.  The inspectors completed one inspection sample.      b.FindingsNo findings of significance were identified.1R05Fire Protection    a.Inspection ScopeThe inspectors walked down accessible portions of the plant described below to assess: (1) the licensee's control of transient combustible material and ignition sources; (2) fire
detection and suppression capabilities; (3) manual firefighting equipment and capability;(4) the condition of passive fire protection features, such as, electrical raceway fire
barrier systems, fire doors, and fire barrier penetrations; and (5) any relatedcompensatory measures.  The inspectors reviewed the Pre-Fire Plan/Strategy Book
during the fire protection inspections.  The areas inspected were:
*Auxiliary building, 70-foot, RHR Pump B Room, fire Area AB-3, on October 11, 2005*Auxiliary building, 95-foot, HPCS piping area, fire Area AB-2/Z-2, on October 12, 2005*Auxiliary building, 95-foot, LPCS panel room, fire Area AB-6/Z33, on October 12, 2005*Control building, 116-foot, safety-related 125 Vdc switchgear room, fireArea C-24, on December 9, 2005*Control building, 116-foot, safety-related Switchgear 1C room, fire Area C-22, onDecember 9, 2005
*Control building, 116-foot, safety-related ENB inverter Charger A room, fireArea C-18, on December 9, 2005The inspectors completed six inspection samples.      b.FindingsNo findings of significance were identified.
Enclosure-8-1R11Licensed Operator Requalification Program    a.Inspection Scope    .1Annual Operating Examination ReviewFollowing the completion of the annual operating examination testing cycle, which endedthe week of September 23, 2005, the inspectors reviewed the overall pass/fail results ofthe annual individual job performance measure operating tests and simulator operating
tests administered by the licensee during the operator licensing requalification cycle. Eight separate crews participated in simulator operating tests and job performance
measure operating tests, totaling 52 licensed operators.  All of the crews tested passed
the simulator portion of the annual operating test.  Two of the 52 licensed operators
failed the job performance measure portion and were successfully remediated.  These
results were compared to the thresholds established in MC 0609, Appendix I, "Operator
Requalification Human Performance Significance Determination Process."  The
inspector completed one inspection sample.      .2Resident Inspector Quarterly ReviewOn November 15, 2005, the inspectors observed simulator training of an operating crew,as part of the operator requalification training program, to assess licensed operator
performance and the training evaluator's critique.  The inspection included observation
of high risk licensed operator actions, operator activities associated with the emergency
plan, and lessons learned from industry and plant experiences.  In addition, the
inspectors compared simulator control panel configurations with the actual control room
panels for consistency.  The simulator examination
scenario observed was
RSMS-OPS-612, "Loss of Vacuum/ATWS/Drywell Steam Leak - RPV Flooding," Revision 4.  The
inspectors completed one
inspection sample.      .3Inadequate Emergency Event Classification Guidance
  On June 10, 2005, the inspectors observed operating crew performance in the simulatorduring annual requalification exam Scenario RSMS-OPS-509, "SRV Tailpipe Steam
Leak Inside The Drywell," Revision 3.  The inspectors discussed crew actions and
emergency planning requirements with the examination evaluators, training
management, emergency planning coordinators, and operations management.  The
inspectors reviewed the following documents:*EIP-2-001, "Classification of Emergencies," Revision 12
*USAR 5.2.5.1.1, "Detection of Leakage within the Drywell"  *Vendor computer manual, VTD-A324-0109, "Analog Devices MICROMAC-5000Final Draft, Leak Rate Detection PLC Documentation, River Bend Station -
Reactor Building Sump Systems," Revision 0
Enclosure-9-*Training Evaluation and Request, TEAR-RBS-2005-0477, "Validating LeakageReport," issued August 23, 2005*CR-RBS-2005-03078, "Validating Leakage Report," initiated on August 26, 2005
*Standing Order Number 192, "Drywell Leakage Greater Than 50 gpm EALGuidance," Revision 0, issued November 3, 2005    b.FindingsIntroduction:  The inspectors identified a Green NCV of 10 CFR Part 50, Appendix E,Section IV.B, for inadequate procedures for implementation of an Alert emergency
action level (EAL). Description:  On June 10 2005, the inspectors observed operating crew performance inthe simulator during annual requalification exam Scenario RSMS-OPS-509, "SRV
Tailpipe Steam Leak Inside The Drywell," Revision 3.  The inspectors noted that when
the examination evaluators informed the team that the total drywell leakage report was84 gpm, the team declared an Alert based on that report.  Procedure EIP-2-001,
"Classification of Emergencies," Revision 12, listed the criteria for an Alert EAL
classification as "Total drywell LEAKAGE greater than 50 gpm." Based on their observations in the simulator, the inspectors questioned the ability of theleakage computer installed in the plant to accurately calculate total drywell leakage
under certain conditions.  The inspectors analyzed the program run by the drywell
leakage computer and determined:  (1) the drywell leakage computer would not
calculate total drywell leakage while a drywell sump pump was running; (2) computer
reports of total drywell leakage printed while a drywell sump pump was running would be
invalid; and (3) if a drywell high pressure or low reactor vessel level signal was present,
the valves in the drywell sump pump discharge lines would close, causing the drywell
sump pumps to run continuously, resulting in an invalid drywell total leakage report.  The
inspectors determined that the indication used by operators to determine if the criteriawas met for declaring an Alert EAL due to total drywell leakage exceeding 50 gpm would
not be valid under certain conditions.On August 23, 2005, the licensee initiated training evaluation action request TEAR-2005-0477 to evaluate this condition to determine what training actions were necessary.
On August 26, 2005, the licensee initiated CR-RBS-2005-03078 that requested analternate means of determining the primary coolant leak Alert EAL using main control
room indications.  The CR also requested additional training materials and classroom
instruction to reinforce this change.On November 3, 2005, the licensee issued Standing Order 192 that provided additionalcriteria to be used to make the determination of whether a primary coolant leak rate
Alert EAL declaration was required, without relying solely on the drywell leakage
computer.  The inspectors concluded that Standing Order 192 was an adequate interim
compensatory measure until the licensee implemented permanent corrective actions.
Enclosure-10-Analysis:  The performance deficiency associated with this finding involved aninadequate procedural criteria for declaring an Alert EAL in the event that total drywell
leakage exceeds 50 gpm under certain conditions.  Specifically, computed drywell
leakrate used by operators to determine if total drywell leakage exceeds 50 gpm may be
invalid under certain conditions.  The finding was more than minor because it is
associated with the Emergency Preparedness Cornerstone attribute of procedural
quality and affects the cornerstone objective to ensure the licensee is capable of
implementing adequate measures to protect the health and safety of the public in the
event of a radiological emergency.  The inadequate procedure could result in a failure to
declare an Alert emergency classification when required.  Using Manual Chapter 0609,
Appendix B, "Emergency Preparedness Significance Determination Process," this
finding was determined to be of very low safety significance since it was a failure to
comply with a regulatory requirement associated with a risk-significant planning
standard that did not result in the loss or degradation of that risk-significant planningstandard function. Enforcement:  The failure to provide adequate procedures for implementation of an EALwas a violation of 10 CFR Part 50, Appendix E, Section IV.B., which requires, in part,
that the licensee's emergency plan describe the means to be used for determining the
impact of the release of radioactive materials including EALs.  Because this finding was
of very low safety significance and was entered into the licensee's corrective action
program as CR-RBS-2005-03078, this violation is being treated as an NCV, consistent
with Section VI.A of the NRC Enforcement Policy:  NCV 05000458/2005005-01, Inadequate procedure for implementation of an EAL.1R13Maintenance Risk Assessments and Emergent Work Control    a.Inspection ScopeThe inspectors reviewed selected maintenance activities to verify the performance ofassessments of plant risk related to planned and emergent maintenance work activities.
The inspectors verified:  (1) the adequacy of the risk assessments and the accuracy and
completeness of the information considered, (2) management of the resultant risk and
implementation of work controls and risk management actions, and (3) effective control
of emergent work, including prompt reassessment of resultant plant risk.  The inspectors
completed three inspection samples.      .1Risk Assessment and Management of RiskOn a routine basis, the inspectors verified performance of risk assessments, inaccordance with administrative Procedure ADM-096, "Risk Management Program
Implementation and On-Line Maintenance Risk Assessment," Revision 04, for planned
maintenance activities and emergent work involving structures, systems, andcomponents within the scope of the maintenance rule.  Specific work activities evaluated
included the following planned and emergent work:*October 23, 2005, Division I residual heat removal and standby service waterequipment outage
Enclosure-11-*November 28, 2005, Division III work week and station blackout diesel generatorplanned maintenance    .2Emergent Work ControlDuring emergent work, the inspectors verified that the licensee took actions to minimizethe probability of initiating events, maintained the functional capability of mitigatingsystems, and maintained barrier integrity.  The inspectors also reviewed the emergentwork activities to ensure the plant was not placed in an unacceptable configuration.  The
specific emergent work activity followed was the cleaning of high voltage insulators in
the main transformer switchyard with a high pressure spray on October 7, 2005.    b.FindingsNo findings of significance were identified.1R14Operator Performance During Nonroutine Evolutions and Events    c.Inspection ScopeThe inspectors completed the two inspection samples listed below.      .1Power Suppression TestingThe inspectors observed portions of and reviewed control room records for powersuppression testing conducted during the weekend of October 21, 2005.  The inspectors
reviewed the reactivity control plan, the prejob briefing given in the main control room at
the beginning of the evolution and during control room operator and reactor engineer
shift turnover.  The inspectors also reviewed the results of the test with the reactor
engineering representative and shift manager, including the recommendation to insert
Control Rod 20-45 to suppress power in the vicinity of a potential leaking fuel bundle.
Finally, the inspectors reviewed the postsuppression test off-gas pretreatment gaseous
activity levels used to monitor the success of the suppression efforts.    .2Trip of Reactor Recirculation (RR) Flow Control Valve (FCV) Hydraulic PowerUnit (HPU)On October 31, 2005, the inspectors observed operator response to a trip of RR FCV BHPU.  As a result, RR FCV B began to drift open.  The operators took action to limit or
stop the gradual opening of RR FCV B.  As RR FCV B continued to open, operators
throttled closed RR FCV A to maintain reactor power less than 100 percent.  These
actions created an RR jet pump loop flow mismatch of greater than 5 percent requiring
entry into TS Action 3.4.1.A.  The inspectors reviewed the TS requirements for this
condition and discussed the actions taken by the operators with the operations shift
Enclosure-12-manager and members of plant management team present in the control room at thetime.  The following documents were reviewed by the inspectors as part of this
inspection:Main Control Room Logs, October 31, 2005CR-RBS-2005-03748, During Filter RCS-FLTR2B replacement, techniciansbumped an electrical cable, causing a trip of the reactor recirculation flow control
Valve B hydraulic power unitW0 00075986, Replace grounded connection to Pressure Switch RCS-PDS90BSOP-0003, Reactor Recirculation System, Revision 35TS limiting condition for operation (LCO) 3.4.1 and applicable Bases    i.FindingsIntroduction:  The inspectors identified a Green noncited violation of TS Action 3.4.1.A.1for the licensee's failure to restore compliance with LCO 3.4.1 or shut down one RR loop
within 2 hours of determining that RR loop jet pump flow mismatch was greater than
5 percent while operating at greater than 70 percent of rated core flow.Description:  On October 31, 2005, at 2:54 p.m., the RR FCV B HPU tripped.  As aresult, RR FCV B began to drift open.  The operators took action to limit or stop the
gradual opening of RR FCV B.  As RR FCV B continued to open, operators throttled
closed RR FCV A to maintain reactor power less than 100 percent.  At 3:06 p.m., the operators entered TS LCO Condition 3.4.1.A because the RR loop jetpump flow mismatch exceeded 5 percent with the plant operating at greater than 70percent rated core flow.  The highest flow mismatch was 8.2 percent.  TS Action
3.4.1.A.1 required the licensee to shut down one recirculation loop with 2 hours.The licensee issued a work request and began to troubleshoot the HPU trip.  At thesame time, operators requested that reactor engineers develop a reactivity control plan
to insert control rods to lower reactor power.  This would allow operators to reopen
RR FCV A to reduce the RR jet pump loop flow mismatch to less than the required
5 percent.  At 4:24 p.m., the licensee determined that the cause for the HPU trip was a blowncontrol power fuse.  The fuse blew as a result of a grounded wire to a filter high
differential pressure switch, which was bumped by maintenance technicians who were
changing the filter cartridge.  The inspectors asked the operators and licensee
management if they intended to shut down one RR loop or perform the actions
necessary to reduce the jet pump flow mismatch to less than 5 percent, as required by
TS 3.4.1.  The licensee responded that they did not want to maneuver the plant andchange core conditions, which might exacerbate the existing condition of two leaking
fuel bundles.
Enclosure-13-At 5:06 p.m., the operators exited TS Action 3.4.1.A without shutting down one RR loopor reducing jet pump loop flow mismatch to less than 5 percent.  Instead they entered
TS Action 3.4.1.D.1, which required that the reactor be placed in Mode 3 in 12 hours. When asked, the operators and licensee management stated that they could commencea plant shutdown within the next 6 hours and still meet the requirement to be in Mode 3in 12 hours.  They also stated that at the 6-hour point, they would commence the
shutdown with the reactivity control plan to reduce reactor power by inserting control
rods and open RR FCV A to reduce jet pump loop flow mismatch to less than 5 percent.
If that was successful, they would then exit TS LCO 3.4.1.Subsequently, the repairs were completed to the pressure switch wire, the control powerfuse was replaced, and RR FCV B HPU was restarted.  Following a one-hour warmup,
the RR FCV B HPU was returned to service.  RR jet pump loop flow was reduced below
5 percent and the licensee exited TS LCO 3.4.1. at 7:36 p.m., 4.5 hours after entry intoTS LCO Condition 3.4.1.A.The inspectors determined that:  (1) when the cause of the trip of RR FCV B HPU wasdetermined to be the grounded pressure switch wire, the licensee knew that the time tomake the repairs and return the HPU to service would exceed the 2-hour completion
time of TS Action 3.4.1.A.1; and (2) the licensee was capable of restoring RR jet pump
loop flow mismatch to less than 5 percent or shutting down one RR loop within the
2-hour completion time of TS Action 3.4.1.A.1. Analysis:  The licensee's failure to restore compliance with TS LCO 3.4.1 or completethe required action of TS 3.4.1.A.1 to shut down one RR loop within 2 hours was aperformance deficiency.  The finding was more than minor because, if left uncorrected,
it would become a more significant safety concern.  According to TS LCO 3.4.1 Bases,
the operation of the RR pumps is an initial condition assumed for the design basis loss-
of-coolant accident (LOCA).  During a LOCA caused by a RR loop break, the intact RR
loop is assumed to provide coolant flow during the first few seconds of the accident.
The initial core flow decrease is rapid because the RR pump in the broken loop ceases
to pump water through the vessel almost immediately.  The pump in the intact loop
coasts down more slowly.  This pump coast down governs the core flow response for
the next several seconds until the jet pump suctions are uncovered.  The analyses
assume that both RR loops are operating at the same flow prior to the LOCA.  However,if the LOCA analysis is reviewed for an initial jet pump flow mismatch with the break
assumed to be in the loop with the higher flow, the flow coast down and core response
are potentially more severe, since the intact loop starts at a lower flow rate. The significance of this finding could not be evaluated using MC 0609, "SignificanceDetermination Process."  Based on management review, the finding was determined to
be of very low safety significance based on the short duration of the flow mismatch,
4.5 hours, and the low likelihood of a LOCA during that time.  The cause of this finding
is related to the cr
osscutting element of human performance in that operators failed toimplement TS requirements. Enforcement:  TS LCO 3.4.1 states that two RR loops shall be in operation withmatched flows when the reactor is in Modes 1 or 2.  If RR loop jet pump flow mismatch
Enclosure-14-is not less than or equal to 5 percent of rated core flow when operating at greater thanor equal to 70 percent of rated core flow (Condition 3.4.1.A), then the licensee must shutdown one RR loop (Required Action A.1) within 2 hours (Completion Time).  Contrary to
the above, on October 31 , 2005, 2 hours after RR loop jet pump flow mismatch was
greater than 5 percent of rated core flow, the licensee exited TS 3.4.1.A.1 withoutshutting down one RR loop or restoring the jet pump flow mismatch to less than
5 percent.  Because the finding is of very low safety significance and has been entered
into the licensee's corrective action program as CR-RBS-2006-00274, this violation is
being treated as an NCV in accordance with Section IV.A of the NRC EnforcementPolicy and is identified as NCV 05000458/2005005-02:  Failure to complete TS required
actions within allowed completion time.1R15Operability Evaluations    a.Inspection ScopeThe inspectors reviewed selected operability determinations on the basis of potentialrisk importance.  The selected samples are addressed in the condition reports (CRs)
listed below.  The inspectors assessed:  (1) the accuracy of the evaluations, (2) the use
and control of compensatory measures if needed, and (3) compliance with TS, the
Technical Requirements Manual, the USAR, and other associated design-basis
documents.  The inspectors' review included a verification that the operabilitydeterminations were made as specified by Entergy Procedure EN-OP-104, "OperabilityDeterminations," Revision 1.  The operability evaluations reviewed were associated with:*CR-RBS-2004-1270, Check valves in primary Containment 113' elevation airlocknot included in the in-service testing program, reviewed on October 11, 2005*CR-RBS-2005-3563, Check valves in primary Containment 113' elevation airlocknot included in the in-service testing procedure, reviewed on October 19, 2005*CR-RBS-2005-3568, In-service test program changed for primary containment113' elevation airlock without changing in-service test procedure, reviewed on
October 19, 2005*CR-RBS-2005-04251, -04252, Safety-related Inverter ENB-INV01B1 frequencyand safety-related instrument Bus VBS-PNL01B voltage out of specification high,
reviewed on December 27, 2005The inspectors completed two inspection samples.      f.FindingsNo findings of significance were identified.
Enclosure-15-1R16Operator Workarounds    a.Inspection ScopeAn operator workaround is defined as a degraded or nonconforming condition thatcomplicates the operation of plant equipment and is compensated for by operatoraction.  During the week of November 28, 2005, the inspectors reviewed an operator
workaround which required operators to hold the control switch for throttle valves for at
least 5 seconds after the full closed indication is received.  The inspectors interviewed
operators to determine if they knew specifically which valves were affected and if they
were aware of this operational requirement from memory.  During the week of December 5, 2005, the inspectors reviewed the cumulative effect ofthe existing operator workarounds on:  (1) the reliability, availability, and potential formisoperation of any mitigati
ng system; (2) whether they could increase the fr equency ofan initiating event; and (3) their effect on the operation of multiple mitigating systems.  Inaddition, the inspectors reviewed the cumulative effects of the operator workarounds on
the ability of the operators to respond in a correct and timely manner to plant transientsand accidents.  The procedures and other documents reviewed by the inspectors were:*Operator Workaround - Control Room Deficiency Program Guidelines,Revision 11
*Operator workaround report*Operator burden report
*Daily plant status reports
*Operations shift turnover sheet
*Standing Order Number 190, "Electrically Operated Throttle Valve Operations,"Revision 0The inspectors completed two inspection samples.      b.FindingsNo findings of significance were identified.1R17Permanent Plant Modifications    a.Inspection ScopeThe inspectors reviewed MR96-0063, "Remove Internals of [Reactor Core IsolationCooling Turbine (RCIC) Exhaust Check Valve] E51-VF040," dated September 18, 1996,
Enclosure-16-and the assumptions made with respect to the capability of the RCIC turbine exhaustline vacuum breaker vent line.  On December 10, 2004, the RCIC turbine was manually
started and ran for a short period of time before shutting down on high reactor water
level.  The RCIC exhaust line drain trap high level alarm came in and operators
observed water draining from the drain trap for 12 hours.  The documents reviewed as
part of this inspection are listed in the attachment.  The inspectors completed one
inspection sample.      b.FindingsIntroduction:  The inspectors identified a self-revealing NCV of 10 CFR Part 50,Appendix B, Criterion III, Design Control, for failure to address a full spectrum of designconditions for the RCIC turbine exhaust line vacuum breaker system as part of a plantmodification to remove the internals of the RCIC turbine exhaust line check valve.  As a
result, on December 10, 2004, when RCIC was started and subsequently shut down on
high reactor water level following a scram and loss of feedwater, the RCIC exhaust line
filled with water from the suppression pool, causing the operators to consider RCIC
unavailable, complicating their response to the event.Description:  In September 1996, in response to a request from mechanicalmaintenance, design engineering processed a design change to remove RCIC Turbine
Exhaust Check Valve E51-VF040.  As part of Modification Request MR-96-0063, an
evaluation was performed on the adequacy of the RCIC turbine exhaust line vacuum
breaker system to prevent the siphoning of suppression pool water into the RCIC turbineexhaust line following a shutdown of the RCIC turbine.  During the evaluation it was
determined that the as-built vacuum breaker vent line was not in accordance with the
original design of the vacuum breaker line.  A new calculation was performed for the
as-built configuration (globe valves and lift check valves versus gate valves and swing
check valves).  The basic assumption used for Calculation PH-056, "RCIC Turbine
Exhaust Line Vacuum Breaker Vent Line Sizing Verification," Revision 1A, was that the
RCIC exhaust line would be at equilibrium conditions when the turbine tripped.  Theturbine would run long enough for the exhausted steam and exhaust piping to be at the
same temperature and that the only cooling effect would be to ambient.  The result was
that the gradual cooldown of the steam and exhaust piping would cause the formation of
a vacuum in approximately 35.5 minutes.  The revised sizing calculation showed that theas-built vacuum breaker vent line was capable of relieving a vacuum created in as short
a time as 3.5 minutes.On December 10, 2004, following a reactor scram, RCIC was started to maintain reactorwater level due to the pending loss of all reactor feed pumps.  When RCIC Steam to
Turbine Valve E51-MOV045 stroked full open, it automatically reclosed due to the high
reactor water level interlock.  It was later determined that steam was admitted to the
turbine for approximately 11 seconds.  As a result, the steam in the exhaust line
condensed more rapidly than assumed and the exhaust line pressure became a vacuum
within 17 seconds.  This rapid pressure reduction overwhelmed the vacuum breaker
vent line and 84 gallons of suppression pool water was siphoned into the RCIC turbine
exhaust line.
Enclosure-17-The licensee later determined that the static and dynamic loads on the turbine exhaustline for a restart on the RCIC turbine would be within design limits, although a water
hammer transient would occur.  Based on test data provided by the turbine
manufacturer, the licensee also determined that the turbine would experience no
damage and not trip on overspeed if it were to be started with water in its exhaust line.
The turbine startup would be slower than normal, but within the assumed values in the
safety analysis.  The turbine exhaust line check valve internals were reinstalled in
February 2005.Analysis:  The failure to adequately address worst case design conditions in the sizingcalculation for the RCIC turbine exhaust line vacuum breaker vent line to allow for the
removal of the exhaust line check valve was a performance deficiency.  The finding was
more than minor because it was associated with the Mitigating Systems cornerstone
attribute of Design Control and affected the cornerstone objective to ensure the
availability and reliability of the RCIC system, a system that responds to initiating events(loss of feedwater and station blackout), to prevent undesirable consequences.  Using
the MC 0609, "Significance Determination Process," Phase 1 Worksheet, the finding
was determined to have very low safety significance because it represented a design
deficiency that did not result in a loss of system function. Enforcement:  10 CFR Part 50, Appendix B, Criterion III, Design Control, states, in part,that design changes, including field changes, shall be subject to design change control
measures commensurate with those applied to the original design.  Contrary to the
above, the RCIC turbine exhaust line vacuum breaker vent line sizing calculation, used
as part of the modification process to remove the exhaust line check valve, did not take
into consideration the most limiting exhaust line conditions.  As a result the vacuum
breaker vent line was not capable of preventing the siphoning of suppression pool water
into the RCIC Turbine Exhaust line.  Because this finding was of very low safety
significance and was documented in the licensee's corrective action program as
CR-RBS-2005-00724, it is being treated as an NCV in accordance with Section IV. A of
the NRC Enforcement Policy and is identified as NCV 05000458/2005005-03:  Inadequate design assumption results in RCIC turbine exhaust header filling with waterfollowing an automatic high water level shutdown.1R19Postmaintenance Testing    a.Inspection ScopeThe inspectors reviewed selected work orders (WO) to ensure that testing activitieswere adequate to verify system operability and functional capability.  The inspectors: (1) identified the safety function(s) for each system by reviewing applicable licensingbasis and/or design-basis documents; (2) reviewed each maintenance activity to identify
which maintenance function(s) may have been affected; (3) reviewed each test
procedure to verify that the procedure did adequately test the safety function(s) that mayhave been affected by the maintenance activity; (4) reviewed the acceptance criteria in
the procedure to ensure consistency with information in the applicable licensing basis
and/or design-basis documents; and (5) identified that the procedure was properlyreviewed and approved.  The eight WOs inspected are listed below:
Enclosure-18-WO 00063768, replace hydrogen igniter in containment dome, review conductedduring the week of October 31, 2005WO 00075881, replace rod control and informati
on system isolation transformer,reviewed during the week of October 31, 2005WO 00074806, rebuild control rod drive Hydraulic Control Unit 4833, reviewconducted during the week of December 12, 2005WO 50969759, rebuild control rod drive Hydraulic Control Unit 1625, reviewconducted during the week of December 12, 2005WO 00066597, rework Inverter BYS-INV01A to fix blown fuse problem, reviewconducted during the week of December 12, 2005WO 50968926, replace frequency detector board on Inverter ENB-INV01B1,review conducted during the week of December 12, 2005WO 00072137, quarterly inspection and lubrication of the station blackout diesel,review conducted during the week of December 19, 2005WO 50967030, clean, inspect, and lubricate the station blackout diesel, reviewconducted during the week of December 19, 2005The inspectors completed eight inspection samples.      b.FindingsNo findings of significance were identified.1R22Surveillance Testing    a.Inspection ScopeThe inspectors verified, by witnessing and reviewing test data, that risk-significantsystem and component surveillance tests met TS, USAR, and procedure requirements. The inspectors ensured that surveillance tests demonstrated that the systems were
capable of performing their intended safety functions and provided operational
readiness.  The inspectors specifically:  (1) evaluated surveillance tests forpreconditioning; (2) evaluated clear acceptance criteria, range, accuracy and current
calibration of test equipment; and (3) verified that equipment was properly restored at
the completion of the testing.  The inspectors observed and reviewed the following
surveillance tests and surveillance test procedures (STP):STP-552-4202, "Post Accident Monitoring/Remote Shutdown System -Suppression Pool Water Level Channel Calibration (CMS-LT23B, CMS-ESX23B,
CMS-LI23B, CMS-TR40B, CMS-LIX23B)," Revision 9A, performed on
October 13, 2005
Enclosure-19-MCP-4303, "Functional Test of Standby Cooling Tower #1 Station BlackoutDivision I Standby Service Water Return Valve and Valve Logic
(SWP-AOV599)," Revision 01A, performed on October 25, 2005STP-552-4502, "Post Accident Monitoring/Remote Shutdown System - DrywellPressure Channel Calibration (CMS-PT2A, CMS-T103, CMS-PR2A),"
Revision 14A, performed on November 28, 2005The inspectors completed three inspection samples.      b.FindingsNo findings of significance were identified.1R23Temporary Plant Modifications    a.Inspection ScopeDuring the week of December 19, 2005, the inspectors reviewed the following temporaryplant modifications:  (1) temporary Alteration TA05-0015-00 to supply Division II safety-
related 120 volt ac electrical distribution Panel SCM-PNL01B from safety-related power
Supply RPS-XRC10B1 so that repairs to safety-related power Supply SCM-XRC14B1
could be made; and (2) temporary Alteration TA05-0014-01 to install radiation shielding
in front of standby gas treatment control Panels GTS-PNL28A/B until a permanent
solution could be installed.  This shielding was installed after an equipment qualification
evaluation showed that the total integrated dose for standby gas treatment Panel GTS-PNL28A/B could exceed qualification doses of internal electrical equipment after the
annulus mixing system was retired.  Specifically, the inspectors:  (1) reviewed eachtemporary modification and its associated 10 CFR 50.59 screening against
the system'sdesign basis documentation, including the USAR and TS; (2) verified that the installationof the temporary modification was consistent with the modification documents; and
(3) reviewed the postinstallation test results to confirm that the actual impact of the
temporary modification on SCM-PNL01B and GTS-PNL28A/B had been adequately
verified.  The inspectors completed two inspection samples.      b.FindingsNo findings of significance were identified.
Cornerstone:  Emergency Preparedness1EP2Alert and Notification System Testing    a.Inspection ScopeThe inspector discussed with licensee staff the status of offsite siren systems todetermine the adequacy of licensee methods for testing the alert and notificati on syst em
Enclosure-20-in accordance with 10 CFR Part 50, Appendix E.  The licensee's alert and notificationsystem testing program was compared with criteria in NUREG-0654, "Criteria forPreparation and Evaluation of Radiological Emergency Response Plans and
Preparedness in Support of Nuclear Power Plants," Revision 1, Federal Emergency
Management Agency (FEMA) Report REP-10, "Guide for the Evaluation of Alert and
Notification Systems for Nuclear Power Plants," and the licensee's current
FEMA-approved alert and notification system design report.  The inspector alsoreviewed Procedures EPP-2-701, "Prompt Notification System Maintenance and
Testing," Revision 18, and EPP-2-401, "Inadvertent Siren Sounding," Revision 7.  Theinspector completed one inspection sample.      b.FindingsNo findings of significance were identified.1EP3Emergency Response Organization Augmentation    a.Inspection ScopeThe inspector reviewed the following documents to determine the licensee's ability tostaff emergency response facilities in accordance with the licensee emergency plan andthe requirements of 10 CFR Part 50, Appendix E.*EIP-2-006, "Notifications," Revision 32*EPP-2-502, "Emergency Communications Equipment Testing," Revision 21
*Details of 10 staffing augmentation and quarterly pager dr
illsThe inspector completed one inspection sample.      b.FindingsNo findings of significance were identified.1EP5Correction of Emergency Preparedness Weaknesses and Deficiencies    a.Inspection ScopeThe inspector reviewed the following documents related to the licensee's correctiveaction program to determine the licensee's ability to identify and correct problems inaccordance with 10 CFR 50.47(b)(14) and 10 CFR Part 50, Appendix E:*Quality assurance audits of the emergency preparedness program conducted in
2003, 2004, and 2005*Four licensee self-assessments
*Licensee evaluation reports for 11 drills and exercises
Enclosure-21-*Summaries of 146 corrective actions assigned to the emergency preparednessdepartment between February 2003 and October 2005*Details of 17 selected CRs
The licensee's corrective action program was also compared with the requirements ofProcedure EN-LI-102, "Corrective Action Process," Revision 2.  The inspector
independently evaluated the emergency operations facility during an October 18, 2005,drill and compared the postdrill critique of licensee performance.  The inspectorcompleted one inspection sample.      b.FindingsNo findings of significance were identified.1EP6Drill Evaluation    a.Inspection ScopeThe inspectors observed the emergency preparedness drill
conducted on October 18,2005, to identify any weaknesses and deficiencies in classification, notification, and
protective action recommendation development activities.  The inspectors also
evaluated the licensee assessment of classification, notification, and protective actionrecommendation development during the drill in accordance with plant procedures andNRC guidelines.  The inspectors also observed the drill evaluator immediate critiques ofthe drill participants classification, notification, and protective action recommendationactivities.  The following procedures and documents were reviewed during the
assessment:EIP-2-001, "Classification of Emergencies," Revision 13EIP-2-006, "Notifications," Revision 32EIP-2-007, "Protective Action Guidelines Recommendations," Revision 21The inspectors completed one
inspection sample.      b.FindingsNo findings of significance were identified.
Enclosure-22-2.RADIATION SAFETYCornerstone:  Occupational Radiation Safety2OS2ALARA Planning and Controls    a.Inspection ScopeThe inspector assessed licensee performance with respect to maintaining individual andcollective radiation exposures as low as is reasonably achievable (ALARA).  The
inspector used the requirements in 10 CFR Part 20 and the licensee's procedures
required by TS as criteria for determining compliance.  The inspector interviewed
licensee personnel and reviewed:*Current 3-year rolling average collective exposure
*Three on-line maintenance work activities scheduled during the inspection periodand associated work activity exposure estimates which were likely to result in the
highest personnel collective exposures*Site-specific ALARA procedures
*ALARA work activity evaluations, exposure estimates, and exposure mitigationrequirements*Intended versus actual work activity doses and the reasons for anyinconsistencies *Dose rate reduction activities in work planning
*Method for adjusting exposure estimates, or replanning work, when unexpectedchanges in scope or emergent work were encountered*Use of engineering controls to achieve dose reductions and dose reductionbenefits afforded by shielding*Radiation worker and radiation protection technician performance during workactivities in radiation areas, airborne radioactivity areas, or high radiation areas *Self-assessments and audits related to the ALARA program since the lastinspection*Corrective action documents related to the ALARA program and follow-upactivities such as initial problem identification, characterization, and trackingThe inspector completed 9 of the required 15 inspection samples and 2 of the optionalinspection samples. 
Enclosure-23-    b.FindingsNo findings of significance were identified.4.OTHER ACTIVITIES
4OA1Performance Indicator VerificationEmergency Preparedness Cornerstone    a.Inspection ScopeThe inspector sampled licensee submittals for the performance indicators listed belowfor the period July 1, 2004, through September 30, 2005.  The definitions and guidanceof NEI 99-02, "Regulatory Assessment Indicator Guideline," Revisions 2 and 3, were
used to verify the licensee's basis for reporting each data element in order to verify the
accuracy of performance indicator data reported during the assessment period.  The
licensee's performance indicator data was also reviewed against the requirements of
Procedure EN-LI-114, "Performance Indicator Process," Revision 0.*Drill and Exercise Performance*Emergency Response Organization Participation
*Alert and Notification System ReliabilityThe inspector reviewed a 100 percent sample of dr
ill and exercise scenarios, licensedoperator simulator training sessions, notification forms, and attendance and critique
records associated with training sessions, drills, and exercises conducted during theverification period.  The inspector reviewed emergency responder qualification, training,
and drill participation records for 20 key licensee emergency response personnel.  Theinspector reviewed procedures for conducting siren testing and a 100 percent sample of
siren test records.  The inspector also interviewed licensee personnel that were
accountable for collecting and evaluating the performance indicator data.The inspector completed three inspection samples.      b.FindingsNo findings of significance were identified.4OA2Identification and Resolution of Problems  1.Emergency Preparedness Annual Sample Review    a.Inspection ScopeThe inspector reviewed a summary listing of 146 corrective actions assigned to theemergency preparedness department, reviewed 17 CRs in detail, and independently
Enclosure-24-assessed the licensee's ability to identify problems associated with an October 18, 2005,integrated drill, in order to assess the licensee's ability to identify and correct problems. The inspector completed one inspection sample.      b.FindingsNo findings of significance were identified.  2.ALARA Planning and Controls Annual Sample Review    a.Inspection ScopeThe inspector evaluated the effectiveness of the licensee's problem identification andresolution processes regarding exposure tracking, higher than planned exposure levels,
and radiation worker practices.  The inspector reviewed the corrective action documents
listed in the attachment against the licensee's problem identification and resolution
program requirements.  The inspector completed one inspection sample.      b.FindingsNo findings of significance were identified.  3.Semiannual Trend Review    a.Inspection ScopeThe inspectors performed a 6-month review of the licensee's corrective action programand associated documents to identify trends that could indicate the existence of a moresignificant safety issue.  The inspector's review was focused on repetitive issues, but
also considered the results of daily inspector screening of CRs and licensee trending
efforts.  The inspector's review considered the six month period of July through
December 2005.  Inspectors reviewed 76 specific CRs and their associated operabilityevaluations.  Operability determinations set the priority for corrective actions to resolve
conditions adverse to quality.  The CR numbers are listed in the attachment.The inspectors also evaluated the CRs and the operability determinations against therequirements of the following guidance documents:*Procedure EN-LI-102, "Corrective Action Process," Revision 1
*Procedure EN-OP-104, "Operability Determinations," Revision 1*Procedure OSP-0040, "LCO Tracking and Safety Function DeterminationProgram," Revision 10*MC 9900, "Operability Determinations and Functionality Assessments forResolution of Degraded or Nonconforming Conditions Adverse to Quality or
Safety," dated September 26, 2005
Enclosure-25-The inspectors completed one inspection sample.      b.Assessment and ObservationsThere were no findings of significance identified.  The inspectors determined that anumber of operability determinations stated that the equipment that was the subject ofthe CR was currently inoperable and being tracked using the LCO Tracking System.
The inspectors found that this system was an effective mechanism for resolution of TSLCOs.  However, from a corrective action program perspective, there was no closure of
the condition adverse to quality (system inoperability) or a discussion of the correctiveactions taken to restore the equipment to operable status in the subject CR.  In addition,
the inspectors observed that a number of operability determinations describedconditions where the system was declared operable but t
he system or a support systemwas in a degraded or nonconforming condition.  In some cases, compensatory actions
were being taken to ensure system operability, but no mechanism was in place toensure that these compensatory measures remained in place until the degraded ornonconforming condition was corrected.  The inspectors did not find any examples
where the nonconforming condition was not corrected within a reasonable period of
time.  4.Resident Inspector Annual Sample ReviewThe inspectors completed two inspection samples.
Ultimate Heat Sink Long Term Heat Removal Capacity    c.Inspection ScopeThe inspectors reviewed CR-RBS-2002-01243, ultimate heat sink capacity less than the30-day requirement, during the week of November 28, 2005.  The inspectors evaluated
the CR against the requirements of the licensee's corrective action program as
described in nuclear management manual Procedure LI-102, "Corrective Action
Process," Revision 4, and 10 CFR Part 50, Appendix B, Criterion XVI.    b. Findings and ObservationsThere were no findings of significance identified.  On August 28, 2002, the inspectorsfound:  (1) the single failure assumption made for the design of the ultimate heat sink
was a trip of standby diesel Generator B immediately after a small line break event, with
bypass, coincident with a loss-of-offsite power and plant trip, (2) the ultimate heat sink
capacity would be less than 30 days if, instead, all ECCS systems worked as designedand no operator actions were taken to secure ECCS, and (3) specific procedures to
replenish the ultimate heat sink during a loss-of-offsite power had not been written.  In
response to the inspectors' concerns, the licensee wrote CR-RBS-2002-01243 and took
the following corrective actions:  (1) revised their procedures to clarify operator actions if
no single failure occurred and to provide instructions for makeup to the ultimate heat
Enclosure-26-sink during a 30-day loss-of-offsite power; and (2) issued license amendment RequestLAR-2001-026, dated March 18, 2003, to revise their TS Bases 3.7, "Standby ServiceWater System and Ultimate Heat Sink," and USAR.Simulator Fidelity Issue Regarding Wide-Range Level Recorders    d.Inspection ScopeThe inspectors reviewed the corrective actions taken by the licensee in response to NCV 05000458/2004005-02, wide-range reactor water level indication did not respond
as expected by operators following an unplanned reactor scram.  On December 10,
2004, a failure of a balance of plant instrument bus caused the feedwater regulatingvalves to fail in their 100 percent flow position.  Following a reactor scram, the feedwater
pumps overfed the reactor and tripped on high reactor water level.  The excess
feedwater caused reactor water level to continue to rise after the feed pump trip.  The
wide-range level recorders' digital output continued to indicate reactor water level
greater than +60 inches, the top end of the wide-range level instruments.  The reactoroperators were not aware that the recorders' digital output would continue to increasebeyond +60 inches because the digital readout of wide-range level recorders in the
simulator stopped at +60 inches.  This response caused some confusion and
complicated the operators' response to the event.  The inspectors reviewed CR-RBS-
2004-04289, -04295, -04296 and -04299 written by the licensee in response to this
event.    e.Findings and ObservationsThere were no findings of significance identified.  The  inspectors found that, when adesign change was implemented changing the wide-range reactor water level recorders
from analog to digital models, the simulator modification made the software for the
recorders stop indicating at the top of scale (+60 inches).  The digital recorders installed
in the control room, however, had no upper limit on the digital indication.  On
December 10, 2004, reactor water level rose above the reference leg tap for the level
transmitter and, as the reference leg condensing chamber cooled down, the wide-range
level transmitters' output continued to increase and the digital indication showed a level
as high as +140 inches.  The inspectors reviewed the corrective actions taken by the
licensee and determined that they were reasonable and adequate to correct the
operator knowledge deficiency caused by the simulator fidelity issue.  The inspectors
interviewed a cross-section of control room operators and determined that the
phenomena was understood and they understood that any wide-range digital indication
greater that +60 inches was invalid and not indicative of actual reactor water level.4OA3Event Followup1.(Closed) Licensee Event Report (LER) 50-458/04-001-00, Automatic Reactor ScramDue to Main Generator Trip Resulting from Switchyard FaultOn August 15, 2004, a transmission tower guy wire failed.  This allowed a 230 kVtransmission line structure between Port Hudson and Fancy Point (Line 353) to fall and
Enclosure-27-create a ground fault condition on the line.  Four breakers in the station switchyard wereslow to open to clear the fault.  As a result:  (1) Reserve Station Transformer 2 was
deenergized, causing a partial loss of off-site power and start of the Division 2
emergency diesel generator; and (2) main transformer protection relays caused a main
generator lockout, which resulted in a generator load reject reactor scram.NRC Integrated Inspection Report 05000458/2004005, issued February 14, 2005,documented a Green, self-revealing finding associated with this event for preconditioned
speed testing of station switchyard breakers and three similar failures of station
switchyard breakers.  The licensee revised the speed testing procedures to avoid
preconditioning the breakers.NRC Supplemental Inspection Report 05000458/2005012, issued October 24, 2005,documented a supplemental inspection performed in accordance with Inspection
Procedure 95001.  The supplemental inspection was in response to four unplanned
reactor scrams that occurred between August 15, 2004, and January 15, 2005.  Thelicensee's root cause analysis identified several programmatic changes which were
incorporated into a switchyard reliability program to improve switchyard maintenancepractices.The inspectors reviewed the LER and the licensee's resolution of identified problemsand determined there were no findings of significance and no other violations of NRC
requirements.  The licensee documented the failed equipment in CR-RBS-2004-02332.4OA6Meetings, Including ExitExit MeetingsOn October 21, 2005, the inspector presented the emergency preparedness inspectionresults to Mr. J. Leavines, Manager, Emergency Planning, and other members of his
staff who acknowledged the findings.  The inspector confirmed that proprietary
information was not provided or examined during the inspection.On November 4, 2005, the inspector presented the licensed operator requalificationprogram inspection results to Mr. Mike Cantrell, Operations Training Supervisor, and
other members of the licensee's management staff.  The licensee acknowledged the
findings presented.  The inspector confirmed that proprietary information was not
provided or examined during the inspection.On December 8, 2005, the inspector presented the ALARA inspection results toMr. R. King, Director, Nuclear Safety Assurance, and other members of his staff who
acknowledged the findings.  The inspector confirmed that proprietary information was
not provided or examined during the inspection.
Enclosure-28-On January 4, 2006, the inspectors presented the integrated baseline inspection resultsto Paul Henninkamp, Vice President, Operations, and other members of licensee
management.  The inspector confirmed that proprietary information was not provided or
examined during the inspection.ATTACHMENT:  SUPPLEMENTAL INFORMATION
A-1AttachmentSUPPLEMENTAL INFORMATIONKEY POINTS OF CONTACTLicensee PersonnelM. Boyle, Manager, Radiation ProtectionD. Burnett, Superintendent, Chemistry
M. Cantrell, Operations Training Supervisor
J. Clark, Assistant Operations Manager - Training
T. Coleman, Manager, Planning and Scheduling/Outage
M. Davis, Acting Manager, Radiation Protection
C. Forpahl, Manager, Corrective Actions
H. Goodman, Director, Engineering
P. Hinnenkamp, Vice President - Operations
B. Houston, Manager, Plant Maintenance
G. Huston, Assistant Operations Manager - Shift
R. King, Director, Nuclear Safety Assurance
J. Leavines, Manager, Emergency Planning
D. Lorfing, Manager, Licensing
J. Maher, Superintendent, Reactor Engineering
W. Mashburn, Manager, Design Engineering
P. Russell, Manager, System Engineering
C. Stafford, Manager, Operations
W. Trudell, Manager, Training and Development
D. Vinci, General Manager - Plant OperationsLIST OF ITEMS OPENED, CLOSED, AND DISCUSSEDOpened and Closed05000458/2005005-01NCVInadequate procedure for implementation of an EAL05000458/2005005-02NCVFailure to complete TS required actions within allowedcompletion time05000458/2005005-03NCVInadequate design assumption results in RCIC turbineexhaust header filling with water following an automatichigh water level shutdownClosed05000458/2004-001-00LERAutomatic Reactor Scram Due to Main Generator TripResulting from Switchyard Fault
A-2AttachmentLIST OF DOCUMENTS REVIEWEDThe following documents were selected and reviewed by the inspectors to accomplish theobjectives and scope of the inspection and to support any findings:Section 1R11:  Licensed Operator Requalification ProgramJob Performance MeasuresRJPM-OPS-052-04, Alternate Control Rod Drive Pumps, August 4, 2005RJPM-OPS-053-03R5, Reset a FCV runback, July 26, 2005
RJPM-OPS-109.4, July 26, 2005
RJPM-OPS-110-04, Synchronize the Main Generator with the Grid, August 2, 2005
RJPM-OPS-256-03R4, Restore level in the SBCT with deepwell pumps, July 26, 2005
RJPM-OPS-309-050, July 19, 2005
RJPM-OPS-508-04, Restore RPS B Normal Power Supply, August 19, 2005
RJPM-OPS-508-07, Respond to reactor scram with control rods failing to insert,August 2, 2005RJPM-OPS-800-17R1, Vent the CCRD over-piston volume, July 26, 2005RJPM-OPS-05206R2, Control rod operability faulted, July 12, 2005RJPM-OPS-05207R2, Alternate control rod drive pumps (Fuel Bldg), July 12, 2005
RJPM-OPS-05304R, Startup A recirc HPU, July 12, 2005
RJPM-OPS-20005R, Perform ATC actions for remote shutdown, August 2, 2005
RJPM-OPS-20006R5, Perform Attachment 13 UO actions, July 26, 2005
ScenariosRSMS-OPS-822, Loss of All Feed Water / RCIC Failure / LOCA, Revision:  00
RSMS-OPS-823, APRM Failure /SRV Failure / EHC Failure / ATWS, Revision:  00
RSMS-OPS-824, LPRM Failure / Loss of Vacuum with MSIV Closure / ATWS,Revision:  00
A-3AttachmentRSMS-OPS-825, Loss of RPS B / Relief Valve Fails Open / Steam Leak in the DrywellWith Failure of the Drywell, Revision:  00RSMS-OPS-827, Rod Drop / Fuel Failure / RCIC Steam Leak / Partial ATWS,Revision:  00RSMS-OPS-829, Failure Of STX-XS2B / Loss Of Condenser Vacuum / ATWS,Revision:  00RSMS-OPS-830, Inadvertent HPCS Injection and Loss of Stator Cooling, Revision:  00Section 1R17:  Permanent Plant ModificationsEvent Notification 41252, Reactor Scram due to Loss of Vital Instrument BusLER 05-458/04-005-01, Unplanned Automatic Scram due to Loss of Non-Vital 120 VoltInstrument Bus, June 22, 2005CR-RBS-2004-04291 RCIC system initiated and subsequently tripped on Level 8CR-RBS-2005-00724 MR96-0063 removed internals from RCIC Turbine Exhaust CheckValve E51-VF040SDRP-P43, System Design Requirements Document, Reactor Core Isolation Cooling,Revision 0SDC-209, Reactor Core Isolation Cooling System Design Criteria, Revision 0,November 9, 1998SDC-209, Reactor Core Isolation Sooling System Design Criteria, Revision 3,September 27, 2004RBS USAR Section 5.4.6, Reactor Core Isolation Cooling System, Revision 17
NUREG-0989, RBS Safety Evaluation Report and Supplements, May 1984 throughOctober 1985GE SIL-30, HPCI/RCIC Turbine Exhaust Line Vacuum Breakers, October 31, 1973
GS AID-56, HPCI/RCI Turbine Exhaust Check Valve Cycling, August 1985
VPF-3622-353 (1) - 1, RCIC Turbine Instruction Manual, January 1975 throughMarch 1978MR96-0063, Remove Internals of [RCIC Exhaust Check Valve] E51-VF040,September 18, 1996
A-4AttachmentCR-RBS-1996-1671, Existing plant configuration of RCIC turbine exhaust line vacuumbreaker vent line does not correspond with configuration assumed in Calculation PH-56,
Revision 0Calculation PH-56, RCIC Turbine Exhaust Line Vacuum Breaker Vent Line SizingVerification, Revision 1A, November 27, 1996Piping and Instrument Drawing PID-27-06A, Reactor Core Isolation Cooling System,Revision 42Calculation G13.18.2.0-079, Determination of Quantity of Water Entering RCIC TurbineExhaust Line, May 11, 2005Calculation G13.18.10.2*225, RCIC Fluid Transient Analysis - Water in Turbine ExhaustLine, May 17, 2005ER-RB-2005-0084-000, Replace Check Valve E51-VF040 or Reinstall Internal Parts,February 20, 2005Terry Turbine SAM-12, Terry Wheel Water Slug Test, March 1, 1973Section 1EP2:  Alert and Notification System TestingRiver Bend Station Emergency Plan, Revision 28River Bend Station Prompt Notification System Design Report, Revision 1,December 2001Section 1EP3:  Emergency Response Organization Augmentation TestingEvaluation Reports for Pager and Augmentation Tests conducted:February 10, 2004June 17, 2004
August 24, 2004
September 23, 2004December 8, 2004January 25, 2005
March 22, 2005July 25, 2005September 27, 2005Section 1EP5:  Correction of Emergency Preparedness Weaknesses and DeficienciesProceduresEN-LI-118, "Root Cause Analysis Process," Revision 1EN-LI-119, "Apparent Cause Evaluation Process," Revision 3
A-5AttachmentQuality AssuranceQuality Assurance Audit Report, QA-7-2003-RBS-1Quality Assurance Audit Report, QA-7-2004-RBS-1
Quality Assurance Audit Report, QA-7-2005-RBS-1Condition ReportsCR-RBS-1999-1316CR-RBS-2003-0586
CR-RBS-2003-0624
CR-RBS-2003-1950
CR-RBS-2003-1992
CR-RBS-2003-2094
CR-RBS-2003-3050
CR-RBS-2004-1090
CR-RBS-2004-1159CR-RBS-2004-3086CR-RBS-2004-3811
CR-RBS-2005-1433
CR-RBS-2005-1602
CR-RBS-2005-1632
CR-RBS-2005-1391
CR-RBS-2005-2516
CR-RBS-2005-2646Evaluation Reports for Drills conductedSeptember 3, 2003March 2 2004
April 20, 2004
May 25, 2004
June 9, 2004
July 27, 2004December 1, 2004 (simulator)December 1, 2004 (medical)
March 24, 2005
April 19, 2005
June 21, 2005Licensee Self-Assessments2004 Evaluated Exercise Pre-AssessmentLO-RLO-2004-00004 CA56, "2004 Long Range ERO Staffing Assessment"
2005 Emergency Planning Program Assessment
Snapshot Assessment of RBS Siren SystemSection 4OA1:  Performance Indicator VerificationProceduresEN-EP-201, "Emergency Planning Performance Indicators," Revision 2EPP-2-703, "Performance Indicators," Revision 2
EIP-2-001, "Classification of Emergencies," Revision 12
EIP-2-002, "Classification Actions," Revision 24
EIP-2-006, "Notifications," Revision 32
EIP-2-007, "Protective Action Recommendation Guidelines," Revision 20
EIP-2-007, "Protective Action Recommendation Guidelines," Revision 21
A-6AttachmentSection 2OS2:  ALARA Planning and ControlsCondition ReportsCR-RBS-2005-01472CR-RBS-2005-01474
CR-RBS-2005-02076CR-RBS-2005-02558CR-RBS-2005-03382
CR-RBS-2005-04004Audits and Self-AssessmentsQA-14-2005-RBS-1Quality Assurance Audit of Radiation Protection SnapshotAssessment /Benchmark on: Effectiveness of the RP TAC/TRG
(July 11-13, 2005)QS-2005-RBS-009ALARA Planning and Controls (August 22 throughSeptember 1, 2005)LO#2005-00123Radiation Protection Program (July 11-15, 2005)
Radiation Work Permits2005-1073Change out filter elements LWS-SKD5-F100A2005-1110Clean-up FB 113' cask pool and install cask pool impact limiter
2005-1310Recirc Flow Control Valve Maintenance ProceduresENS-RP-105Radiation Work Permits, Revision 7RP-110ALARA Program, Revision 2ALARA Committee MinutesAMC 05-01January 11, 2005AMC 05-02January 12, 2005
AMC 05-03January 17, 2005
AMC 05-11July 14, 2005Section 4OA2:  Identification and Resolution of ProblemsCondition reportsCR-RBS-2005-02444CR-RBS-2005-02481
CR-RBS-2005-02486
CR-RBS-2005-02494
CR-RBS-2005-02548
CR-RBS-2005-02563CR-RBS-2005-02570CR-RBS-2005-02590
CR-RBS-2005-02605
CR-RBS-2005-02621
CR-RBS-2005-02624
CR-RBS-2005-02626
A-7AttachmentCR-RBS-2005-02645CR-RBS-2005-02649
CR-RBS-2005-02659
CR-RBS-2005-02664
CR-RBS-2005-02686
CR-RBS-2005-02693
CR-RBS-2005-02695
CR-RBS-2005-02722
CR-RBS-2005-02724
CR-RBS-2005-02727
CR-RBS-2005-02738
CR-RBS-2005-02754
CR-RBS-2005-02760
CR-RBS-2005-02767
CR-RBS-2005-02768
CR-RBS-2005-03106
CR-RBS-2005-03111
CR-RBS-2005-03114
CR-RBS-2005-03125
CR-RBS-2005-03131
CR-RBS-2005-03138
CR-RBS-2005-03151
CR-RBS-2005-03152
CR-RBS-2005-03165
CR-RBS-2005-03178
CR-RBS-2005-03182
CR-RBS-2005-03220
CR-RBS-2005-03242
CR-RBS-2005-03265
CR-RBS-2005-03273
CR-RBS-2005-03279
CR-RBS-2005-03443CR-RBS-2005-03446CR-RBS-2005-03471
CR-RBS-2005-03474
CR-RBS-2005-03503
CR-RBS-2005-03509
CR-RBS-2005-03513
CR-RBS-2005-03515
CR-RBS-2005-03554
CR-RBS-2005-03586
CR-RBS-2005-03594
CR-RBS-2005-03619
CR-RBS-2005-03629
CR-RBS-2005-03645
CR-RBS-2005-03670
CR-RBS-2005-03706
CR-RBS-2005-03728
CR-RBS-2005-03747
CR-RBS-2005-03753
CR-RBS-2005-03787
CR-RBS-2005-03831
CR-RBS-2005-03847
CR-RBS-2005-03887
CR-RBS-2005-03918
CR-RBS-2005-03948
CR-RBS-2005-03969
CR-RBS-2005-04018
CR-RBS-2005-04064
CR-RBS-2005-04071
CR-RBS-2005-04095
CR-RBS-2005-04103
CR-RBS-2005-04106
CR-RBS-2005-04118
A-8AttachmentLIST OF ACRONYMSALARAas low as is reasonably achievable
CFRCode of Federal RegulationsCRcondition report
CR-RBSRiver Bend Station condition report
EALemergency action level
FEMAFederal Emergency Management Agency
FCVflow control valve
HPUhydraulic power unit
MCmanual chapter
LERlicensee event report
LCOlimiting condition for operation
LOCAloss of coolant accident
NCVnoncited violation
NEINuclear Energy Institute
NRCU.S. Nuclear Regulatory Commission
RCICreactor core isolation cooling system
RCSreactor coolant system
RRreactor recirculation system
SOPsystem operating proceduresSTPsurveillance test procedure
TSTechnical Specification
USARUpdated Safety Analysis Report
WOwork order
}}

Revision as of 00:32, 14 July 2019

IR 05000458-05-005; on 10/01/2005 - 12/31/2005; River Bend Station; Licensed Operator Requalification, Operator Performance During Nonroutine Plant Evolutions, Permanent Plant Modifications
ML060450209
Person / Time
Site: River Bend Entergy icon.png
Issue date: 02/13/2006
From: Kennedy K
NRC/RGN-IV/DRP/RPB-C
To: Hinnenkamp P
Entergy Operations
References
IR-05-005
Download: ML060450209 (41)


See also: IR 05000458/2005005

Text

February 13, 2006Paul D. HinnenkampVice President - Operations

Entergy Operations, Inc.

River Bend Station

5485 US Highway 61N

St. Francisville, Louisiana 70775SUBJECT:RIVER BEND STATION - NRC INTEGRATED INSPECTIONREPORT 05000458/2005005Dear Mr. Hinnenkamp:

On December 31, 2005, the U.S. Nuclear Regulatory Commission (NRC) completed aninspection at your River Bend Station. The enclosed integrated inspection report documentsthe inspection findings which were discussed with you and other members of your staff on

January 4, 2006.The inspection examined activities conducted under your license as they relate to safety andcompliance with the Commission's rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.Based on the results of this inspection, two NRC identified findings and one self-revealingfinding were evaluated under the risk significance determination process as having very low

safety significance (Green). The NRC has also determined that violations are associated withthese findings. However, because these violations were of very low safety significance and

were entered into your corrective action program, the NRC is treating these violations as

noncited violations, consistent with Section VI.A.1 of the NRC's Enforcement Policy. If youcontest the violations or the significance of the violations, you should provide a response within30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear

Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, withcopies to the Regional Administrator, U.S. Nuclear Regulatory Commission, Region IV, 611

Ryan Plaza Drive, Suite 400, Arlington, Texas 76011-4005; the Director, Office of Enforcement,U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resi dentInspector at the River Bend Station facility.In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, itsenclosure, and your response (if any) will be available electronically for public inspection in theNRC Public Document Room or from the Publicly Available Records (PARS) com

ponent ofNRC's document system (ADAMS). ADAMS is accessible from the NRC Website at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Entergy Operations, Inc.-2-Should you have any questions concerning this inspection, we will be pleased to discuss themwith you.Sincerely,/RA/Kriss M. Kennedy, ChiefProject Branch C

Division of Reactor ProjectsDocket: 50-458License: NPF-47Enclosures:NRC Inspection Report 05000458/2005005 w/Attachment: Supplemental Informationcc w/enclosure:Senior Vice President and

Chief Operating Officer

Entergy Operations, Inc.

P.O. Box 31995

Jackson, MS 39286-1995Vice President Operations Support

Entergy Operations, Inc.

P.O. Box 31995

Jackson, MS 39286-1995General ManagerPlant Operations

Entergy Operations, Inc.

River Bend Station

5485 US Highway 61N

St. Francisville, LA

70775Director - Nuclear SafetyEntergy Operations, Inc.

River Bend Station

5485 US Highway 61N

St. Francisville, LA

70775

Entergy Operations, Inc.-3-Wise, Carter, Child & Caraway

P.O. Box 651

Jackson, MS 39205Winston & Strawn LLP1700 K Street, N.W.

Washington, DC 20006-3817Manager - LicensingEntergy Operations, Inc.

River Bend Station

5485 US Highway 61N

St. Francisville, LA

70775The Honorable Charles C. Foti, Jr.Attorney General

Department of Justice

State of Louisiana

P.O. Box 94005

Baton Rouge, LA 70804-9005H. Anne Plettinger

3456 Villa Rose DriveBaton Rouge, LA 70806Burt Babers, PresidentWest Feliciana Parish Police Jury

P.O. Box 1921

St. Francisville, LA

70775Michael E. Henry, State Liaison OfficerDepartment of Environmental Quality

Permits Division

P.O. Box 4313

Baton Rouge, LA 70821-4313Brian AlmonPublic Utility Commission

William B. Travis Building

P.O. Box 13326

1701 North Congress Avenue

Austin, TX 78711-3326

Entergy Operations, Inc.-4-ChairpersonDenton Field Office

Chemical and Nuclear Preparedness

and Protection Division

Office of Infrastructure Protection

Preparedness Directorate

Dept. of Homeland Security

800 North Loop 288

Federal Regional Center

Denton, TX 76201-3698

Entergy Operations, Inc.-5-Electronic distribution by RIV:Regional Administrator (BSM1)DRP Director (ATH)DRS Director (DDC)DRS Deputy Director (RJC1)Senior Resident Inspector (PJA)Branch Chief, DRP/C (KMK)Senior Project Engineer, DRP/C (WCW)Team Leader, DRP/TSS (RLN1)RITS Coordinator (KEG)DRS STA (DAP)J. Dixon-Herrity, OEDO RIV Coordinator (JLD)ROPreports

RBS Site Secretary (LGD)W. A. Maier, RSLO (WAM)SUNSI Review Completed: _kmk_ADAMS: Yes G No Initials: __kmk__ Publicly Available

G Non-Publicly Available

G Sensitive Non-SensitiveR:\_REACTORS\_RB\2005\RB2005-05RP-PJA.wpdRIV:SRI:DRP/CRI:DRP/CC:DRS/OBC:DRS/EB1C:DRS/PSBPJAlterMOMillerATGodyJClarkMPS

hannon T - KMKennedy E - KMKennedy /RA/ /RA/ /RA/2/ /062/ /062/ /062/ /062/ /06C:DRS/EB2C:DRP/CLJSmithKMKennedy GDReplogle for /RA/2/13/062/13/06OFFICIAL RECORD COPY T=Telephone E=E-mail F=Fax

Enclosure-1-U.S. NUCLEAR REGULATORY COMMISSIONREGION IVDocket:50-458License:NPF-47

Report:05000458/2005005

Licensee:Entergy Operations, Inc.

Facility:River Bend StationLocation:5485 U.S. Highway 61St. Francisville, LouisianaDates:October 1 through December 31, 2005

Inspectors:P. Alter, Senior Resident Inspector, Project Branch CM. Miller, Resident Inspector, Project Branch CJ. Keeton, Consultant, Region IV

P. Elkmann, Emergency Preparedness Inspector, Operations Branch

G. Johnston, Senior Operations Engineer, Operations Branch

L. Ricketson, Senior Health Physicist, Plant Support BranchApproved By:Kriss M. Kennedy, ChiefProject Branch C

Division of Reactor Projects

Enclosure-2-TABLE OF CONTENTSSUMMARY OF FINDINGS....................................................3REPORT DETAILS..........................................................5

REACTOR SAFETY.........................................................51R01Adverse Weather Protection

.......................................51R04Equipment Alignment

.............................................61R05Fire Protection

..................................................71R11Licensed Operator Requalification

...................................81R13Maintenance Risk Assessments and Emergent Work Control.............101R14Operator Performance During Non-routine Plant Evolutions..............111R15Operability Evaluations..........................................141R16Operator Work-Arounds.........................................151R17Permanent Plant Modifications....................................151R19Postmaintenance Testing........................................171R22Surveillance Testing............................................181R23Temporary Plant Modifications....................................191EP2Alert and Notification System Testing...............................191EP3Emergency Response Organization Augmentation.....................201EP5Correction of Emergency Preparedness Weaknesses and Deficiencies.....201EP6Drill Evaluation.................................................21RADIATION SAFETY.......................................................222OS2ALARA Planning and Controls.....................................22OTHER ACTIVITIES........................................................234OA1Performance Indicator Verification..................................234OA2Identification and Resolution of Problems............................234OA3Event Followup................................................264OA6Meetings, Including Exit..........................................27SUPPLEMENTAL INFORMATION............................................A-1

KEY POINTS OF CONTACT................................................A-1

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED...........................A-1LIST OF DOCUMENTS REVIEWED..........................................A-2

LIST OF ACRONYMS......................................................A-8

Enclosure-3-SUMMARY OF FINDINGSIR 05000458/2005005; 10/01/2005 - 12/31/2005; River Bend Station; Licensed OperatorRequalification, Operator Performance During Nonroutine Plant Evolutions, Permanent PlantModifications.The report covered a 3-month period of routine baseline inspections by resident inspectors andannounced baseline inspections by regional emergency planning, operations, and radiation

protection inspectors. Three Green noncited violations were identified. The significance of

most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual

Chapter 0609, "Significance Determination Process." Findings for which the significance

determination process does not apply may be Green or be assigned a severity level after NRC

management review. The NRC's program for overseeing the safe operation of commercialnuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 3,dated July 2000.A.NRC-Identified and Self-Revealing FindingsCornerstone: Initiating Events*Green. The NRC identified a noncited violation of Technical Specification 3.4.1.A for thelicensee's failure to shut down one reactor recirculation loop within 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> of

determining that jet pump loop flow mismatch was greater than 5 percent whileoperating at greater than 70 percent of rated core flow. On October 31, 2005, theReactor Recirculation Flow Control Valve B hydraulic power unit tripped because of a

blown control power fuse, causing Flow Control Valve B to drift open. Operators

throttled closed Flow Control Valve A to maintain reactor power at 100 percent, resulting

in a jet pump loop flow mismatch of approximately 8.2 percent. The flow mismatch

existed for 4.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />. The licensee entered this into their corrective action program as

Condition Report CR-RBS-2006-00274. The finding was more than minor because, if left uncorrected, it would become a moresignificant safety concern. Matched recirculation loop flows is an assumption used in

the accident analysis for a loss of coolant accident resulting from a loop break. A flow

mismatch could result in core response that is more severe than assumed in the

accident analysis. The significance of this finding could not be evaluated using

MC 0609, "Significance Determination Process." Based on management review, the

finding was determined to be of very low safety significance based on the short duration

of the flow mismatch, 4.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />, and the low likelihood of a loss of coolant accident

during that time. The cause of this finding is related to the crosscutting element ofhuman performance in that operators failed to implement Technical Specification

requirements (Section 1R14).Cornerstone: Mitigating Systems

III,Design Control, was identified for the licensee's failure to address the worst case

conditions in the sizing calculation for the reactor core isolation cooling turbine exhaust

Enclosure-4-line vacuum breaker system as part of a plant modification to remove the internals of thereactor core isolation cooling turbine exhaust line check valve. As a result, on

December 10, 2004, when the reactor core isolation cooling system was started andsubsequently shutdown on high reactor water level following a scram and loss of

feedwater, the turbine exhaust line filled with water from the suppression pool, causingthe operators to consider t

he system unavailable and complicating their response to theevent. The licensee entered this finding into their corrective action program as CR-

RBS-2005-00724 and reinstalled the turbine exhaust line check valve internals in

February 2005. The finding was more than minor because it was associated with the Mitigating Systemscornerstone attribute of Design Control and affected the cornerstone objective to ensure

the availability and reliability of the reactor core isolation cooling system, a system thatresponds to initiating events (loss of feedwater and station blackout), to prevent

undesirable consequences. Using Manual Chapter 0609, "Significance Determination

Process," Phase 1 Worksheet, the finding was determined to have very low safety

significance because it represented a design deficiency that did not result in a loss of

system function (Section 1R17).Cornerstone: Emergency Preparedness

  • Green. The NRC identified a noncited violation of 10 CFR Part 50, Appendix E,Section IV. B., as a result of inadequate procedures for the implementation of an

emergency action level. The criteria in Procedure EIP-2-001, "Classification of

Emergencies," Revision 12, for declaring an Alert emergency action level based on

primary coolant leak rate, relied solely on a computer generated leakrate report that

would not be valid under all conditions. The licensee entered this finding into their

corrective action program as CR-RBS-2005-03078 and issued Standing Order 192, as

an interim corrective action, to provide additional criteria to determine whether a primary

coolant leak rate Alert emergency action level declaration was required.The finding is more than minor because it is associated with the EmergencyPreparedness Cornerstone attribute of procedural quality and affects the cornerstone

objective to ensure the licensee is capable of implementing adequate measures to

protect the health and safety of the public in the event of a radiological emergency. The

inadequate procedure could result in a failure to declare an Alert emergency

classification when required. Using Manual Chapter 0609, Appendix B, "Emergency

Preparedness Significance Determination Process," this finding was determined to be of

very low safety significance since it was a failure to comply with a regulatory

requirement associated with a risk-significant planning standard that did not result in the

loss or degradation of that risk-significant planning standard function (Section 1R11).B.Licensee-Identified Violations

None.

Enclosure-5-REPORT DETAILSSummary of Plant Status

On October 1, 2005, reactor power was lowered to 70 percent to perform a rod sequenceexchange and insert two control rods for planned maintenance. The reactor was returned to

100 percent power on October 2, 2005. On October 21, 2005, reactor power was lowered to 63percent to perform power suppression testing for a leaking fuel bundle. The reactor was

returned to 100 percent power on October 23, 2005. On November 5, 2005, reactor power was

lowered to 90 percent to adjust the control rod pattern and the reactor was returned to 100

percent later that day. On December 2, 2005, reactor power was lowered to 83 percent to

insert three control rods for planned maintenance. The reactor was returned to 100 percent

power on December 3, 2005. On December 9, 2005, reactor power was lowered to 58 percent

to perform a control rod pattern adjustment and conduct turbine valve testing. The reactor was

returned to 100 percent power on December 11, 2005. On December 17, 2005, reactor power

was lowered to 62 percent to perform power suppression testing for a leaking fuel bundle. The

reactor was returned to 100 percent on December 19, 2005, and remained at 100 percent for

the remainder of the inspection period.1.REACTOR SAFETYCornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, EmergencyPreparedness1R01Adverse Weather Protection b.Inspection ScopeCold Weather PreparationDuring the week of December 5, 2005, the inspectors reviewed the licensee'simplementation of Operations Section Procedure OSP-0043, "Freeze Protection andTemperature Maintenance," Revision 6, to protect mitigating systems from cold weatherconditions. Specifically, the inspectors: (1) verified that risk-significant structures,

systems, and components will remain functional when challenged by cold weatherconditions; (2) verified that cold weather features such as heat tracing and space

heaters are operable and monitored; and (3) verified that the cold weather proceduresattachments were being completed for changing temperatures as required by the

procedure. The inspectors completed one inspection sample. c.FindingsNo findings of significance were identified.

Enclosure-6-1R04Equipment Alignment 1.Partial System Walkdowns a.Inspection Scope

On October 25, 2005, the inspectors walked down residual heat removal Division II

while residual heat removal Division I was out of service for scheduled maintenance.

On October 26, 2005, the inspectors walked down the piping and valve lineup of the

condensate storage tank, including emergency core cooling system suction and testreturn valves. In each case, the inspectors verified the correct valve and power

alignments by comparing positions of valves, switches, and electrical power breakers to

the system operating procedures (SOP) and piping and instrument drawings listedbelow and applicable sections of the Updated Safety Analysis Report (USAR). The

inspectors completed two inspection samples. *SOP-0031, "Residual Heat Removal System," Revision 46

  • SOP-0008, "Condensate Storage, Makeup and Transfer," Revision 16
  • Piping and Instrument PID 04-03A, "Condensate Storage, Makeup andTransfer," Revision 13 b.FindingsNo findings of significance were identified. 2.Complete System Walkdown a.Inspection ScopeThe inspectors conducted a complete walkdown of the drywell and containment leakdetection system during the week of June 26, 2005, during a drywell closeout inspectionand continuing the week of November 20, 2005. The methods of inspection included

field walkdown, in-office reviews, observation of system operation, and interviews ofcomputer engineering, operations, training, and emergency planning personnel. The

inspectors verified: (1) proper valve and control switch alignments, (2) computer

program algorithm, (3) power supply lineup, (4) associated support system st

atus, and(5) that alarms and indications in the main control room were as specified in the

following documents:*SOP-0033, "Drywell and Containment Leak Detection System," Revision 11*USAR Section 5.2.5.1.1, "Detection of Leakage within the Drywell"*Technical Specifications (TS) Section 3.4.5, "RCS Operational Leakage"The inspectors also verified electrical power requirements, labeling, hangers andsupport installation, and associated support systems status. The walkdowns included

Enclosure-7-evaluation of system piping and supports to ensure (1) piping and pipe supports did notshow evidence of damage, (2) hangers were secure, and (3) component foundations

were not degraded. The inspectors completed one inspection sample. b.FindingsNo findings of significance were identified.1R05Fire Protection a.Inspection ScopeThe inspectors walked down accessible portions of the plant described below to assess: (1) the licensee's control of transient combustible material and ignition sources; (2) fire

detection and suppression capabilities; (3) manual firefighting equipment and capability;(4) the condition of passive fire protection features, such as, electrical raceway fire

barrier systems, fire doors, and fire barrier penetrations; and (5) any relatedcompensatory measures. The inspectors reviewed the Pre-Fire Plan/Strategy Book

during the fire protection inspections. The areas inspected were:

  • Auxiliary building, 70-foot, RHR Pump B Room, fire Area AB-3, on October 11, 2005*Auxiliary building, 95-foot, HPCS piping area, fire Area AB-2/Z-2, on October 12, 2005*Auxiliary building, 95-foot, LPCS panel room, fire Area AB-6/Z33, on October 12, 2005*Control building, 116-foot, safety-related 125 Vdc switchgear room, fireArea C-24, on December 9, 2005*Control building, 116-foot, safety-related Switchgear 1C room, fire Area C-22, onDecember 9, 2005
  • Control building, 116-foot, safety-related ENB inverter Charger A room, fireArea C-18, on December 9, 2005The inspectors completed six inspection samples. b.FindingsNo findings of significance were identified.

Enclosure-8-1R11Licensed Operator Requalification Program a.Inspection Scope .1Annual Operating Examination ReviewFollowing the completion of the annual operating examination testing cycle, which endedthe week of September 23, 2005, the inspectors reviewed the overall pass/fail results ofthe annual individual job performance measure operating tests and simulator operating

tests administered by the licensee during the operator licensing requalification cycle. Eight separate crews participated in simulator operating tests and job performance

measure operating tests, totaling 52 licensed operators. All of the crews tested passed

the simulator portion of the annual operating test. Two of the 52 licensed operators

failed the job performance measure portion and were successfully remediated. These

results were compared to the thresholds established in MC 0609, Appendix I, "Operator

Requalification Human Performance Significance Determination Process." The

inspector completed one inspection sample. .2Resident Inspector Quarterly ReviewOn November 15, 2005, the inspectors observed simulator training of an operating crew,as part of the operator requalification training program, to assess licensed operator

performance and the training evaluator's critique. The inspection included observation

of high risk licensed operator actions, operator activities associated with the emergency

plan, and lessons learned from industry and plant experiences. In addition, the

inspectors compared simulator control panel configurations with the actual control room

panels for consistency. The simulator examination

scenario observed was

RSMS-OPS-612, "Loss of Vacuum/ATWS/Drywell Steam Leak - RPV Flooding," Revision 4. The

inspectors completed one

inspection sample. .3Inadequate Emergency Event Classification Guidance

On June 10, 2005, the inspectors observed operating crew performance in the simulatorduring annual requalification exam Scenario RSMS-OPS-509, "SRV Tailpipe Steam

Leak Inside The Drywell," Revision 3. The inspectors discussed crew actions and

emergency planning requirements with the examination evaluators, training

management, emergency planning coordinators, and operations management. The

inspectors reviewed the following documents:*EIP-2-001, "Classification of Emergencies," Revision 12

  • USAR 5.2.5.1.1, "Detection of Leakage within the Drywell" *Vendor computer manual, VTD-A324-0109, "Analog Devices MICROMAC-5000Final Draft, Leak Rate Detection PLC Documentation, River Bend Station -

Reactor Building Sump Systems," Revision 0

Enclosure-9-*Training Evaluation and Request, TEAR-RBS-2005-0477, "Validating LeakageReport," issued August 23, 2005*CR-RBS-2005-03078, "Validating Leakage Report," initiated on August 26, 2005

  • Standing Order Number 192, "Drywell Leakage Greater Than 50 gpm EALGuidance," Revision 0, issued November 3, 2005 b.FindingsIntroduction: The inspectors identified a Green NCV of 10 CFR Part 50, Appendix E,Section IV.B, for inadequate procedures for implementation of an Alert emergency

action level (EAL). Description: On June 10 2005, the inspectors observed operating crew performance inthe simulator during annual requalification exam Scenario RSMS-OPS-509, "SRV

Tailpipe Steam Leak Inside The Drywell," Revision 3. The inspectors noted that when

the examination evaluators informed the team that the total drywell leakage report was84 gpm, the team declared an Alert based on that report. Procedure EIP-2-001,

"Classification of Emergencies," Revision 12, listed the criteria for an Alert EAL

classification as "Total drywell LEAKAGE greater than 50 gpm." Based on their observations in the simulator, the inspectors questioned the ability of theleakage computer installed in the plant to accurately calculate total drywell leakage

under certain conditions. The inspectors analyzed the program run by the drywell

leakage computer and determined: (1) the drywell leakage computer would not

calculate total drywell leakage while a drywell sump pump was running; (2) computer

reports of total drywell leakage printed while a drywell sump pump was running would be

invalid; and (3) if a drywell high pressure or low reactor vessel level signal was present,

the valves in the drywell sump pump discharge lines would close, causing the drywell

sump pumps to run continuously, resulting in an invalid drywell total leakage report. The

inspectors determined that the indication used by operators to determine if the criteriawas met for declaring an Alert EAL due to total drywell leakage exceeding 50 gpm would

not be valid under certain conditions.On August 23, 2005, the licensee initiated training evaluation action request TEAR-2005-0477 to evaluate this condition to determine what training actions were necessary.

On August 26, 2005, the licensee initiated CR-RBS-2005-03078 that requested analternate means of determining the primary coolant leak Alert EAL using main control

room indications. The CR also requested additional training materials and classroom

instruction to reinforce this change.On November 3, 2005, the licensee issued Standing Order 192 that provided additionalcriteria to be used to make the determination of whether a primary coolant leak rate

Alert EAL declaration was required, without relying solely on the drywell leakage

computer. The inspectors concluded that Standing Order 192 was an adequate interim

compensatory measure until the licensee implemented permanent corrective actions.

Enclosure-10-Analysis: The performance deficiency associated with this finding involved aninadequate procedural criteria for declaring an Alert EAL in the event that total drywell

leakage exceeds 50 gpm under certain conditions. Specifically, computed drywell

leakrate used by operators to determine if total drywell leakage exceeds 50 gpm may be

invalid under certain conditions. The finding was more than minor because it is

associated with the Emergency Preparedness Cornerstone attribute of procedural

quality and affects the cornerstone objective to ensure the licensee is capable of

implementing adequate measures to protect the health and safety of the public in the

event of a radiological emergency. The inadequate procedure could result in a failure to

declare an Alert emergency classification when required. Using Manual Chapter 0609,

Appendix B, "Emergency Preparedness Significance Determination Process," this

finding was determined to be of very low safety significance since it was a failure to

comply with a regulatory requirement associated with a risk-significant planning

standard that did not result in the loss or degradation of that risk-significant planningstandard function. Enforcement: The failure to provide adequate procedures for implementation of an EALwas a violation of 10 CFR Part 50, Appendix E, Section IV.B., which requires, in part,

that the licensee's emergency plan describe the means to be used for determining the

impact of the release of radioactive materials including EALs. Because this finding was

of very low safety significance and was entered into the licensee's corrective action

program as CR-RBS-2005-03078, this violation is being treated as an NCV, consistent

with Section VI.A of the NRC Enforcement Policy: NCV 05000458/2005005-01, Inadequate procedure for implementation of an EAL.1R13Maintenance Risk Assessments and Emergent Work Control a.Inspection ScopeThe inspectors reviewed selected maintenance activities to verify the performance ofassessments of plant risk related to planned and emergent maintenance work activities.

The inspectors verified: (1) the adequacy of the risk assessments and the accuracy and

completeness of the information considered, (2) management of the resultant risk and

implementation of work controls and risk management actions, and (3) effective control

of emergent work, including prompt reassessment of resultant plant risk. The inspectors

completed three inspection samples. .1Risk Assessment and Management of RiskOn a routine basis, the inspectors verified performance of risk assessments, inaccordance with administrative Procedure ADM-096, "Risk Management Program

Implementation and On-Line Maintenance Risk Assessment," Revision 04, for planned

maintenance activities and emergent work involving structures, systems, andcomponents within the scope of the maintenance rule. Specific work activities evaluated

included the following planned and emergent work:*October 23, 2005, Division I residual heat removal and standby service waterequipment outage

Enclosure-11-*November 28, 2005, Division III work week and station blackout diesel generatorplanned maintenance .2Emergent Work ControlDuring emergent work, the inspectors verified that the licensee took actions to minimizethe probability of initiating events, maintained the functional capability of mitigatingsystems, and maintained barrier integrity. The inspectors also reviewed the emergentwork activities to ensure the plant was not placed in an unacceptable configuration. The

specific emergent work activity followed was the cleaning of high voltage insulators in

the main transformer switchyard with a high pressure spray on October 7, 2005. b.FindingsNo findings of significance were identified.1R14Operator Performance During Nonroutine Evolutions and Events c.Inspection ScopeThe inspectors completed the two inspection samples listed below. .1Power Suppression TestingThe inspectors observed portions of and reviewed control room records for powersuppression testing conducted during the weekend of October 21, 2005. The inspectors

reviewed the reactivity control plan, the prejob briefing given in the main control room at

the beginning of the evolution and during control room operator and reactor engineer

shift turnover. The inspectors also reviewed the results of the test with the reactor

engineering representative and shift manager, including the recommendation to insert

Control Rod 20-45 to suppress power in the vicinity of a potential leaking fuel bundle.

Finally, the inspectors reviewed the postsuppression test off-gas pretreatment gaseous

activity levels used to monitor the success of the suppression efforts. .2Trip of Reactor Recirculation (RR) Flow Control Valve (FCV) Hydraulic PowerUnit (HPU)On October 31, 2005, the inspectors observed operator response to a trip of RR FCV BHPU. As a result, RR FCV B began to drift open. The operators took action to limit or

stop the gradual opening of RR FCV B. As RR FCV B continued to open, operators

throttled closed RR FCV A to maintain reactor power less than 100 percent. These

actions created an RR jet pump loop flow mismatch of greater than 5 percent requiring

entry into TS Action 3.4.1.A. The inspectors reviewed the TS requirements for this

condition and discussed the actions taken by the operators with the operations shift

Enclosure-12-manager and members of plant management team present in the control room at thetime. The following documents were reviewed by the inspectors as part of this

inspection:Main Control Room Logs, October 31, 2005CR-RBS-2005-03748, During Filter RCS-FLTR2B replacement, techniciansbumped an electrical cable, causing a trip of the reactor recirculation flow control

Valve B hydraulic power unitW0 00075986, Replace grounded connection to Pressure Switch RCS-PDS90BSOP-0003, Reactor Recirculation System, Revision 35TS limiting condition for operation (LCO) 3.4.1 and applicable Bases i.FindingsIntroduction: The inspectors identified a Green noncited violation of TS Action 3.4.1.A.1for the licensee's failure to restore compliance with LCO 3.4.1 or shut down one RR loop

within 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> of determining that RR loop jet pump flow mismatch was greater than

5 percent while operating at greater than 70 percent of rated core flow.Description: On October 31, 2005, at 2:54 p.m., the RR FCV B HPU tripped. As aresult, RR FCV B began to drift open. The operators took action to limit or stop the

gradual opening of RR FCV B. As RR FCV B continued to open, operators throttled

closed RR FCV A to maintain reactor power less than 100 percent. At 3:06 p.m., the operators entered TS LCO Condition 3.4.1.A because the RR loop jetpump flow mismatch exceeded 5 percent with the plant operating at greater than 70percent rated core flow. The highest flow mismatch was 8.2 percent. TS Action

3.4.1.A.1 required the licensee to shut down one recirculation loop with 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />.The licensee issued a work request and began to troubleshoot the HPU trip. At thesame time, operators requested that reactor engineers develop a reactivity control plan

to insert control rods to lower reactor power. This would allow operators to reopen

RR FCV A to reduce the RR jet pump loop flow mismatch to less than the required

5 percent. At 4:24 p.m., the licensee determined that the cause for the HPU trip was a blowncontrol power fuse. The fuse blew as a result of a grounded wire to a filter high

differential pressure switch, which was bumped by maintenance technicians who were

changing the filter cartridge. The inspectors asked the operators and licensee

management if they intended to shut down one RR loop or perform the actions

necessary to reduce the jet pump flow mismatch to less than 5 percent, as required by

TS 3.4.1. The licensee responded that they did not want to maneuver the plant andchange core conditions, which might exacerbate the existing condition of two leaking

fuel bundles.

Enclosure-13-At 5:06 p.m., the operators exited TS Action 3.4.1.A without shutting down one RR loopor reducing jet pump loop flow mismatch to less than 5 percent. Instead they entered

TS Action 3.4.1.D.1, which required that the reactor be placed in Mode 3 in 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />. When asked, the operators and licensee management stated that they could commencea plant shutdown within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and still meet the requirement to be in Mode 3in 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />. They also stated that at the 6-hour point, they would commence the

shutdown with the reactivity control plan to reduce reactor power by inserting control

rods and open RR FCV A to reduce jet pump loop flow mismatch to less than 5 percent.

If that was successful, they would then exit TS LCO 3.4.1.Subsequently, the repairs were completed to the pressure switch wire, the control powerfuse was replaced, and RR FCV B HPU was restarted. Following a one-hour warmup,

the RR FCV B HPU was returned to service. RR jet pump loop flow was reduced below

5 percent and the licensee exited TS LCO 3.4.1. at 7:36 p.m., 4.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> after entry intoTS LCO Condition 3.4.1.A.The inspectors determined that: (1) when the cause of the trip of RR FCV B HPU wasdetermined to be the grounded pressure switch wire, the licensee knew that the time tomake the repairs and return the HPU to service would exceed the 2-hour completion

time of TS Action 3.4.1.A.1; and (2) the licensee was capable of restoring RR jet pump

loop flow mismatch to less than 5 percent or shutting down one RR loop within the

2-hour completion time of TS Action 3.4.1.A.1. Analysis: The licensee's failure to restore compliance with TS LCO 3.4.1 or completethe required action of TS 3.4.1.A.1 to shut down one RR loop within 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> was aperformance deficiency. The finding was more than minor because, if left uncorrected,

it would become a more significant safety concern. According to TS LCO 3.4.1 Bases,

the operation of the RR pumps is an initial condition assumed for the design basis loss-

of-coolant accident (LOCA). During a LOCA caused by a RR loop break, the intact RR

loop is assumed to provide coolant flow during the first few seconds of the accident.

The initial core flow decrease is rapid because the RR pump in the broken loop ceases

to pump water through the vessel almost immediately. The pump in the intact loop

coasts down more slowly. This pump coast down governs the core flow response for

the next several seconds until the jet pump suctions are uncovered. The analyses

assume that both RR loops are operating at the same flow prior to the LOCA. However,if the LOCA analysis is reviewed for an initial jet pump flow mismatch with the break

assumed to be in the loop with the higher flow, the flow coast down and core response

are potentially more severe, since the intact loop starts at a lower flow rate. The significance of this finding could not be evaluated using MC 0609, "SignificanceDetermination Process." Based on management review, the finding was determined to

be of very low safety significance based on the short duration of the flow mismatch,

4.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />, and the low likelihood of a LOCA during that time. The cause of this finding

is related to the cr

osscutting element of human performance in that operators failed toimplement TS requirements. Enforcement: TS LCO 3.4.1 states that two RR loops shall be in operation withmatched flows when the reactor is in Modes 1 or 2. If RR loop jet pump flow mismatch

Enclosure-14-is not less than or equal to 5 percent of rated core flow when operating at greater thanor equal to 70 percent of rated core flow (Condition 3.4.1.A), then the licensee must shutdown one RR loop (Required Action A.1) within 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> (Completion Time). Contrary to

the above, on October 31 , 2005, 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> after RR loop jet pump flow mismatch was

greater than 5 percent of rated core flow, the licensee exited TS 3.4.1.A.1 withoutshutting down one RR loop or restoring the jet pump flow mismatch to less than

5 percent. Because the finding is of very low safety significance and has been entered

into the licensee's corrective action program as CR-RBS-2006-00274, this violation is

being treated as an NCV in accordance with Section IV.A of the NRC EnforcementPolicy and is identified as NCV 05000458/2005005-02: Failure to complete TS required

actions within allowed completion time.1R15Operability Evaluations a.Inspection ScopeThe inspectors reviewed selected operability determinations on the basis of potentialrisk importance. The selected samples are addressed in the condition reports (CRs)

listed below. The inspectors assessed: (1) the accuracy of the evaluations, (2) the use

and control of compensatory measures if needed, and (3) compliance with TS, the

Technical Requirements Manual, the USAR, and other associated design-basis

documents. The inspectors' review included a verification that the operabilitydeterminations were made as specified by Entergy Procedure EN-OP-104, "OperabilityDeterminations," Revision 1. The operability evaluations reviewed were associated with:*CR-RBS-2004-1270, Check valves in primary Containment 113' elevation airlocknot included in the in-service testing program, reviewed on October 11, 2005*CR-RBS-2005-3563, Check valves in primary Containment 113' elevation airlocknot included in the in-service testing procedure, reviewed on October 19, 2005*CR-RBS-2005-3568, In-service test program changed for primary containment113' elevation airlock without changing in-service test procedure, reviewed on

October 19, 2005*CR-RBS-2005-04251, -04252, Safety-related Inverter ENB-INV01B1 frequencyand safety-related instrument Bus VBS-PNL01B voltage out of specification high,

reviewed on December 27, 2005The inspectors completed two inspection samples. f.FindingsNo findings of significance were identified.

Enclosure-15-1R16Operator Workarounds a.Inspection ScopeAn operator workaround is defined as a degraded or nonconforming condition thatcomplicates the operation of plant equipment and is compensated for by operatoraction. During the week of November 28, 2005, the inspectors reviewed an operator

workaround which required operators to hold the control switch for throttle valves for at

least 5 seconds after the full closed indication is received. The inspectors interviewed

operators to determine if they knew specifically which valves were affected and if they

were aware of this operational requirement from memory. During the week of December 5, 2005, the inspectors reviewed the cumulative effect ofthe existing operator workarounds on: (1) the reliability, availability, and potential formisoperation of any mitigati

ng system; (2) whether they could increase the fr equency ofan initiating event; and (3) their effect on the operation of multiple mitigating systems. Inaddition, the inspectors reviewed the cumulative effects of the operator workarounds on

the ability of the operators to respond in a correct and timely manner to plant transientsand accidents. The procedures and other documents reviewed by the inspectors were:*Operator Workaround - Control Room Deficiency Program Guidelines,Revision 11

  • Operator workaround report*Operator burden report
  • Daily plant status reports
  • Operations shift turnover sheet
  • Standing Order Number 190, "Electrically Operated Throttle Valve Operations,"Revision 0The inspectors completed two inspection samples. b.FindingsNo findings of significance were identified.1R17Permanent Plant Modifications a.Inspection ScopeThe inspectors reviewed MR96-0063, "Remove Internals of [Reactor Core IsolationCooling Turbine (RCIC) Exhaust Check Valve] E51-VF040," dated September 18, 1996,

Enclosure-16-and the assumptions made with respect to the capability of the RCIC turbine exhaustline vacuum breaker vent line. On December 10, 2004, the RCIC turbine was manually

started and ran for a short period of time before shutting down on high reactor water

level. The RCIC exhaust line drain trap high level alarm came in and operators

observed water draining from the drain trap for 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />. The documents reviewed as

part of this inspection are listed in the attachment. The inspectors completed one

inspection sample. b.FindingsIntroduction: The inspectors identified a self-revealing NCV of 10 CFR Part 50,Appendix B, Criterion III, Design Control, for failure to address a full spectrum of designconditions for the RCIC turbine exhaust line vacuum breaker system as part of a plantmodification to remove the internals of the RCIC turbine exhaust line check valve. As a

result, on December 10, 2004, when RCIC was started and subsequently shut down on

high reactor water level following a scram and loss of feedwater, the RCIC exhaust line

filled with water from the suppression pool, causing the operators to consider RCIC

unavailable, complicating their response to the event.Description: In September 1996, in response to a request from mechanicalmaintenance, design engineering processed a design change to remove RCIC Turbine

Exhaust Check Valve E51-VF040. As part of Modification Request MR-96-0063, an

evaluation was performed on the adequacy of the RCIC turbine exhaust line vacuum

breaker system to prevent the siphoning of suppression pool water into the RCIC turbineexhaust line following a shutdown of the RCIC turbine. During the evaluation it was

determined that the as-built vacuum breaker vent line was not in accordance with the

original design of the vacuum breaker line. A new calculation was performed for the

as-built configuration (globe valves and lift check valves versus gate valves and swing

check valves). The basic assumption used for Calculation PH-056, "RCIC Turbine

Exhaust Line Vacuum Breaker Vent Line Sizing Verification," Revision 1A, was that the

RCIC exhaust line would be at equilibrium conditions when the turbine tripped. Theturbine would run long enough for the exhausted steam and exhaust piping to be at the

same temperature and that the only cooling effect would be to ambient. The result was

that the gradual cooldown of the steam and exhaust piping would cause the formation of

a vacuum in approximately 35.5 minutes. The revised sizing calculation showed that theas-built vacuum breaker vent line was capable of relieving a vacuum created in as short

a time as 3.5 minutes.On December 10, 2004, following a reactor scram, RCIC was started to maintain reactorwater level due to the pending loss of all reactor feed pumps. When RCIC Steam to

Turbine Valve E51-MOV045 stroked full open, it automatically reclosed due to the high

reactor water level interlock. It was later determined that steam was admitted to the

turbine for approximately 11 seconds. As a result, the steam in the exhaust line

condensed more rapidly than assumed and the exhaust line pressure became a vacuum

within 17 seconds. This rapid pressure reduction overwhelmed the vacuum breaker

vent line and 84 gallons of suppression pool water was siphoned into the RCIC turbine

exhaust line.

Enclosure-17-The licensee later determined that the static and dynamic loads on the turbine exhaustline for a restart on the RCIC turbine would be within design limits, although a water

hammer transient would occur. Based on test data provided by the turbine

manufacturer, the licensee also determined that the turbine would experience no

damage and not trip on overspeed if it were to be started with water in its exhaust line.

The turbine startup would be slower than normal, but within the assumed values in the

safety analysis. The turbine exhaust line check valve internals were reinstalled in

February 2005.Analysis: The failure to adequately address worst case design conditions in the sizingcalculation for the RCIC turbine exhaust line vacuum breaker vent line to allow for the

removal of the exhaust line check valve was a performance deficiency. The finding was

more than minor because it was associated with the Mitigating Systems cornerstone

attribute of Design Control and affected the cornerstone objective to ensure the

availability and reliability of the RCIC system, a system that responds to initiating events(loss of feedwater and station blackout), to prevent undesirable consequences. Using

the MC 0609, "Significance Determination Process," Phase 1 Worksheet, the finding

was determined to have very low safety significance because it represented a design

deficiency that did not result in a loss of system function. Enforcement: 10 CFR Part 50, Appendix B, Criterion III, Design Control, states, in part,that design changes, including field changes, shall be subject to design change control

measures commensurate with those applied to the original design. Contrary to the

above, the RCIC turbine exhaust line vacuum breaker vent line sizing calculation, used

as part of the modification process to remove the exhaust line check valve, did not take

into consideration the most limiting exhaust line conditions. As a result the vacuum

breaker vent line was not capable of preventing the siphoning of suppression pool water

into the RCIC Turbine Exhaust line. Because this finding was of very low safety

significance and was documented in the licensee's corrective action program as

CR-RBS-2005-00724, it is being treated as an NCV in accordance with Section IV. A of

the NRC Enforcement Policy and is identified as NCV 05000458/2005005-03: Inadequate design assumption results in RCIC turbine exhaust header filling with waterfollowing an automatic high water level shutdown.1R19Postmaintenance Testing a.Inspection ScopeThe inspectors reviewed selected work orders (WO) to ensure that testing activitieswere adequate to verify system operability and functional capability. The inspectors: (1) identified the safety function(s) for each system by reviewing applicable licensingbasis and/or design-basis documents; (2) reviewed each maintenance activity to identify

which maintenance function(s) may have been affected; (3) reviewed each test

procedure to verify that the procedure did adequately test the safety function(s) that mayhave been affected by the maintenance activity; (4) reviewed the acceptance criteria in

the procedure to ensure consistency with information in the applicable licensing basis

and/or design-basis documents; and (5) identified that the procedure was properlyreviewed and approved. The eight WOs inspected are listed below:

Enclosure-18-WO 00063768, replace hydrogen igniter in containment dome, review conductedduring the week of October 31, 2005WO 00075881, replace rod control and informati

on system isolation transformer,reviewed during the week of October 31, 2005WO 00074806, rebuild control rod drive Hydraulic Control Unit 4833, reviewconducted during the week of December 12, 2005WO 50969759, rebuild control rod drive Hydraulic Control Unit 1625, reviewconducted during the week of December 12, 2005WO 00066597, rework Inverter BYS-INV01A to fix blown fuse problem, reviewconducted during the week of December 12, 2005WO 50968926, replace frequency detector board on Inverter ENB-INV01B1,review conducted during the week of December 12, 2005WO 00072137, quarterly inspection and lubrication of the station blackout diesel,review conducted during the week of December 19, 2005WO 50967030, clean, inspect, and lubricate the station blackout diesel, reviewconducted during the week of December 19, 2005The inspectors completed eight inspection samples. b.FindingsNo findings of significance were identified.1R22Surveillance Testing a.Inspection ScopeThe inspectors verified, by witnessing and reviewing test data, that risk-significantsystem and component surveillance tests met TS, USAR, and procedure requirements. The inspectors ensured that surveillance tests demonstrated that the systems were

capable of performing their intended safety functions and provided operational

readiness. The inspectors specifically: (1) evaluated surveillance tests forpreconditioning; (2) evaluated clear acceptance criteria, range, accuracy and current

calibration of test equipment; and (3) verified that equipment was properly restored at

the completion of the testing. The inspectors observed and reviewed the following

surveillance tests and surveillance test procedures (STP):STP-552-4202, "Post Accident Monitoring/Remote Shutdown System -Suppression Pool Water Level Channel Calibration (CMS-LT23B, CMS-ESX23B,

CMS-LI23B, CMS-TR40B, CMS-LIX23B)," Revision 9A, performed on

October 13, 2005

Enclosure-19-MCP-4303, "Functional Test of Standby Cooling Tower #1 Station BlackoutDivision I Standby Service Water Return Valve and Valve Logic

(SWP-AOV599)," Revision 01A, performed on October 25, 2005STP-552-4502, "Post Accident Monitoring/Remote Shutdown System - DrywellPressure Channel Calibration (CMS-PT2A, CMS-T103, CMS-PR2A),"

Revision 14A, performed on November 28, 2005The inspectors completed three inspection samples. b.FindingsNo findings of significance were identified.1R23Temporary Plant Modifications a.Inspection ScopeDuring the week of December 19, 2005, the inspectors reviewed the following temporaryplant modifications: (1) temporary Alteration TA05-0015-00 to supply Division II safety-

related 120 volt ac electrical distribution Panel SCM-PNL01B from safety-related power

Supply RPS-XRC10B1 so that repairs to safety-related power Supply SCM-XRC14B1

could be made; and (2) temporary Alteration TA05-0014-01 to install radiation shielding

in front of standby gas treatment control Panels GTS-PNL28A/B until a permanent

solution could be installed. This shielding was installed after an equipment qualification

evaluation showed that the total integrated dose for standby gas treatment Panel GTS-PNL28A/B could exceed qualification doses of internal electrical equipment after the

annulus mixing system was retired. Specifically, the inspectors: (1) reviewed eachtemporary modification and its associated 10 CFR 50.59 screening against

the system'sdesign basis documentation, including the USAR and TS; (2) verified that the installationof the temporary modification was consistent with the modification documents; and

(3) reviewed the postinstallation test results to confirm that the actual impact of the

temporary modification on SCM-PNL01B and GTS-PNL28A/B had been adequately

verified. The inspectors completed two inspection samples. b.FindingsNo findings of significance were identified.

Cornerstone: Emergency Preparedness1EP2Alert and Notification System Testing a.Inspection ScopeThe inspector discussed with licensee staff the status of offsite siren systems todetermine the adequacy of licensee methods for testing the alert and notificati on syst em

Enclosure-20-in accordance with 10 CFR Part 50, Appendix E. The licensee's alert and notificationsystem testing program was compared with criteria in NUREG-0654, "Criteria forPreparation and Evaluation of Radiological Emergency Response Plans and

Preparedness in Support of Nuclear Power Plants," Revision 1, Federal Emergency

Management Agency (FEMA) Report REP-10, "Guide for the Evaluation of Alert and

Notification Systems for Nuclear Power Plants," and the licensee's current

FEMA-approved alert and notification system design report. The inspector alsoreviewed Procedures EPP-2-701, "Prompt Notification System Maintenance and

Testing," Revision 18, and EPP-2-401, "Inadvertent Siren Sounding," Revision 7. Theinspector completed one inspection sample. b.FindingsNo findings of significance were identified.1EP3Emergency Response Organization Augmentation a.Inspection ScopeThe inspector reviewed the following documents to determine the licensee's ability tostaff emergency response facilities in accordance with the licensee emergency plan andthe requirements of 10 CFR Part 50, Appendix E.*EIP-2-006, "Notifications," Revision 32*EPP-2-502, "Emergency Communications Equipment Testing," Revision 21

  • Details of 10 staffing augmentation and quarterly pager dr

illsThe inspector completed one inspection sample. b.FindingsNo findings of significance were identified.1EP5Correction of Emergency Preparedness Weaknesses and Deficiencies a.Inspection ScopeThe inspector reviewed the following documents related to the licensee's correctiveaction program to determine the licensee's ability to identify and correct problems inaccordance with 10 CFR 50.47(b)(14) and 10 CFR Part 50, Appendix E:*Quality assurance audits of the emergency preparedness program conducted in

2003, 2004, and 2005*Four licensee self-assessments

  • Licensee evaluation reports for 11 drills and exercises

Enclosure-21-*Summaries of 146 corrective actions assigned to the emergency preparednessdepartment between February 2003 and October 2005*Details of 17 selected CRs

The licensee's corrective action program was also compared with the requirements ofProcedure EN-LI-102, "Corrective Action Process," Revision 2. The inspector

independently evaluated the emergency operations facility during an October 18, 2005,drill and compared the postdrill critique of licensee performance. The inspectorcompleted one inspection sample. b.FindingsNo findings of significance were identified.1EP6Drill Evaluation a.Inspection ScopeThe inspectors observed the emergency preparedness drill

conducted on October 18,2005, to identify any weaknesses and deficiencies in classification, notification, and

protective action recommendation development activities. The inspectors also

evaluated the licensee assessment of classification, notification, and protective actionrecommendation development during the drill in accordance with plant procedures andNRC guidelines. The inspectors also observed the drill evaluator immediate critiques ofthe drill participants classification, notification, and protective action recommendationactivities. The following procedures and documents were reviewed during the

assessment:EIP-2-001, "Classification of Emergencies," Revision 13EIP-2-006, "Notifications," Revision 32EIP-2-007, "Protective Action Guidelines Recommendations," Revision 21The inspectors completed one

inspection sample. b.FindingsNo findings of significance were identified.

Enclosure-22-2.RADIATION SAFETYCornerstone: Occupational Radiation Safety2OS2ALARA Planning and Controls a.Inspection ScopeThe inspector assessed licensee performance with respect to maintaining individual andcollective radiation exposures as low as is reasonably achievable (ALARA). The

inspector used the requirements in 10 CFR Part 20 and the licensee's procedures

required by TS as criteria for determining compliance. The inspector interviewed

licensee personnel and reviewed:*Current 3-year rolling average collective exposure

  • Three on-line maintenance work activities scheduled during the inspection periodand associated work activity exposure estimates which were likely to result in the

highest personnel collective exposures*Site-specific ALARA procedures

  • ALARA work activity evaluations, exposure estimates, and exposure mitigationrequirements*Intended versus actual work activity doses and the reasons for anyinconsistencies *Dose rate reduction activities in work planning
  • Method for adjusting exposure estimates, or replanning work, when unexpectedchanges in scope or emergent work were encountered*Use of engineering controls to achieve dose reductions and dose reductionbenefits afforded by shielding*Radiation worker and radiation protection technician performance during workactivities in radiation areas, airborne radioactivity areas, or high radiation areas *Self-assessments and audits related to the ALARA program since the lastinspection*Corrective action documents related to the ALARA program and follow-upactivities such as initial problem identification, characterization, and trackingThe inspector completed 9 of the required 15 inspection samples and 2 of the optionalinspection samples.

Enclosure-23- b.FindingsNo findings of significance were identified.4.OTHER ACTIVITIES

4OA1Performance Indicator VerificationEmergency Preparedness Cornerstone a.Inspection ScopeThe inspector sampled licensee submittals for the performance indicators listed belowfor the period July 1, 2004, through September 30, 2005. The definitions and guidanceof NEI 99-02, "Regulatory Assessment Indicator Guideline," Revisions 2 and 3, were

used to verify the licensee's basis for reporting each data element in order to verify the

accuracy of performance indicator data reported during the assessment period. The

licensee's performance indicator data was also reviewed against the requirements of

Procedure EN-LI-114, "Performance Indicator Process," Revision 0.*Drill and Exercise Performance*Emergency Response Organization Participation

  • Alert and Notification System ReliabilityThe inspector reviewed a 100 percent sample of dr

ill and exercise scenarios, licensedoperator simulator training sessions, notification forms, and attendance and critique

records associated with training sessions, drills, and exercises conducted during theverification period. The inspector reviewed emergency responder qualification, training,

and drill participation records for 20 key licensee emergency response personnel. Theinspector reviewed procedures for conducting siren testing and a 100 percent sample of

siren test records. The inspector also interviewed licensee personnel that were

accountable for collecting and evaluating the performance indicator data.The inspector completed three inspection samples. b.FindingsNo findings of significance were identified.4OA2Identification and Resolution of Problems 1.Emergency Preparedness Annual Sample Review a.Inspection ScopeThe inspector reviewed a summary listing of 146 corrective actions assigned to theemergency preparedness department, reviewed 17 CRs in detail, and independently

Enclosure-24-assessed the licensee's ability to identify problems associated with an October 18, 2005,integrated drill, in order to assess the licensee's ability to identify and correct problems. The inspector completed one inspection sample. b.FindingsNo findings of significance were identified. 2.ALARA Planning and Controls Annual Sample Review a.Inspection ScopeThe inspector evaluated the effectiveness of the licensee's problem identification andresolution processes regarding exposure tracking, higher than planned exposure levels,

and radiation worker practices. The inspector reviewed the corrective action documents

listed in the attachment against the licensee's problem identification and resolution

program requirements. The inspector completed one inspection sample. b.FindingsNo findings of significance were identified. 3.Semiannual Trend Review a.Inspection ScopeThe inspectors performed a 6-month review of the licensee's corrective action programand associated documents to identify trends that could indicate the existence of a moresignificant safety issue. The inspector's review was focused on repetitive issues, but

also considered the results of daily inspector screening of CRs and licensee trending

efforts. The inspector's review considered the six month period of July through

December 2005. Inspectors reviewed 76 specific CRs and their associated operabilityevaluations. Operability determinations set the priority for corrective actions to resolve

conditions adverse to quality. The CR numbers are listed in the attachment.The inspectors also evaluated the CRs and the operability determinations against therequirements of the following guidance documents:*Procedure EN-LI-102, "Corrective Action Process," Revision 1

Safety," dated September 26, 2005

Enclosure-25-The inspectors completed one inspection sample. b.Assessment and ObservationsThere were no findings of significance identified. The inspectors determined that anumber of operability determinations stated that the equipment that was the subject ofthe CR was currently inoperable and being tracked using the LCO Tracking System.

The inspectors found that this system was an effective mechanism for resolution of TSLCOs. However, from a corrective action program perspective, there was no closure of

the condition adverse to quality (system inoperability) or a discussion of the correctiveactions taken to restore the equipment to operable status in the subject CR. In addition,

the inspectors observed that a number of operability determinations describedconditions where the system was declared operable but t

he system or a support systemwas in a degraded or nonconforming condition. In some cases, compensatory actions

were being taken to ensure system operability, but no mechanism was in place toensure that these compensatory measures remained in place until the degraded ornonconforming condition was corrected. The inspectors did not find any examples

where the nonconforming condition was not corrected within a reasonable period of

time. 4.Resident Inspector Annual Sample ReviewThe inspectors completed two inspection samples.

Ultimate Heat Sink Long Term Heat Removal Capacity c.Inspection ScopeThe inspectors reviewed CR-RBS-2002-01243, ultimate heat sink capacity less than the30-day requirement, during the week of November 28, 2005. The inspectors evaluated

the CR against the requirements of the licensee's corrective action program as

described in nuclear management manual Procedure LI-102, "Corrective Action

Process," Revision 4, and 10 CFR Part 50, Appendix B, Criterion XVI. b. Findings and ObservationsThere were no findings of significance identified. On August 28, 2002, the inspectorsfound: (1) the single failure assumption made for the design of the ultimate heat sink

was a trip of standby diesel Generator B immediately after a small line break event, with

bypass, coincident with a loss-of-offsite power and plant trip, (2) the ultimate heat sink

capacity would be less than 30 days if, instead, all ECCS systems worked as designedand no operator actions were taken to secure ECCS, and (3) specific procedures to

replenish the ultimate heat sink during a loss-of-offsite power had not been written. In

response to the inspectors' concerns, the licensee wrote CR-RBS-2002-01243 and took

the following corrective actions: (1) revised their procedures to clarify operator actions if

no single failure occurred and to provide instructions for makeup to the ultimate heat

Enclosure-26-sink during a 30-day loss-of-offsite power; and (2) issued license amendment RequestLAR-2001-026, dated March 18, 2003, to revise their TS Bases 3.7, "Standby ServiceWater System and Ultimate Heat Sink," and USAR.Simulator Fidelity Issue Regarding Wide-Range Level Recorders d.Inspection ScopeThe inspectors reviewed the corrective actions taken by the licensee in response to NCV 05000458/2004005-02, wide-range reactor water level indication did not respond

as expected by operators following an unplanned reactor scram. On December 10,

2004, a failure of a balance of plant instrument bus caused the feedwater regulatingvalves to fail in their 100 percent flow position. Following a reactor scram, the feedwater

pumps overfed the reactor and tripped on high reactor water level. The excess

feedwater caused reactor water level to continue to rise after the feed pump trip. The

wide-range level recorders' digital output continued to indicate reactor water level

greater than +60 inches, the top end of the wide-range level instruments. The reactoroperators were not aware that the recorders' digital output would continue to increasebeyond +60 inches because the digital readout of wide-range level recorders in the

simulator stopped at +60 inches. This response caused some confusion and

complicated the operators' response to the event. The inspectors reviewed CR-RBS-

2004-04289, -04295, -04296 and -04299 written by the licensee in response to this

event. e.Findings and ObservationsThere were no findings of significance identified. The inspectors found that, when adesign change was implemented changing the wide-range reactor water level recorders

from analog to digital models, the simulator modification made the software for the

recorders stop indicating at the top of scale (+60 inches). The digital recorders installed

in the control room, however, had no upper limit on the digital indication. On

December 10, 2004, reactor water level rose above the reference leg tap for the level

transmitter and, as the reference leg condensing chamber cooled down, the wide-range

level transmitters' output continued to increase and the digital indication showed a level

as high as +140 inches. The inspectors reviewed the corrective actions taken by the

licensee and determined that they were reasonable and adequate to correct the

operator knowledge deficiency caused by the simulator fidelity issue. The inspectors

interviewed a cross-section of control room operators and determined that the

phenomena was understood and they understood that any wide-range digital indication

greater that +60 inches was invalid and not indicative of actual reactor water level.4OA3Event Followup1.(Closed) Licensee Event Report (LER) 50-458/04-001-00, Automatic Reactor ScramDue to Main Generator Trip Resulting from Switchyard FaultOn August 15, 2004, a transmission tower guy wire failed. This allowed a 230 kVtransmission line structure between Port Hudson and Fancy Point (Line 353) to fall and

Enclosure-27-create a ground fault condition on the line. Four breakers in the station switchyard wereslow to open to clear the fault. As a result: (1) Reserve Station Transformer 2 was

deenergized, causing a partial loss of off-site power and start of the Division 2

emergency diesel generator; and (2) main transformer protection relays caused a main

generator lockout, which resulted in a generator load reject reactor scram.NRC Integrated Inspection Report 05000458/2004005, issued February 14, 2005,documented a Green, self-revealing finding associated with this event for preconditioned

speed testing of station switchyard breakers and three similar failures of station

switchyard breakers. The licensee revised the speed testing procedures to avoid

preconditioning the breakers.NRC Supplemental Inspection Report 05000458/2005012, issued October 24, 2005,documented a supplemental inspection performed in accordance with Inspection

Procedure 95001. The supplemental inspection was in response to four unplanned

reactor scrams that occurred between August 15, 2004, and January 15, 2005. Thelicensee's root cause analysis identified several programmatic changes which were

incorporated into a switchyard reliability program to improve switchyard maintenancepractices.The inspectors reviewed the LER and the licensee's resolution of identified problemsand determined there were no findings of significance and no other violations of NRC

requirements. The licensee documented the failed equipment in CR-RBS-2004-02332.4OA6Meetings, Including ExitExit MeetingsOn October 21, 2005, the inspector presented the emergency preparedness inspectionresults to Mr. J. Leavines, Manager, Emergency Planning, and other members of his

staff who acknowledged the findings. The inspector confirmed that proprietary

information was not provided or examined during the inspection.On November 4, 2005, the inspector presented the licensed operator requalificationprogram inspection results to Mr. Mike Cantrell, Operations Training Supervisor, and

other members of the licensee's management staff. The licensee acknowledged the

findings presented. The inspector confirmed that proprietary information was not

provided or examined during the inspection.On December 8, 2005, the inspector presented the ALARA inspection results toMr. R. King, Director, Nuclear Safety Assurance, and other members of his staff who

acknowledged the findings. The inspector confirmed that proprietary information was

not provided or examined during the inspection.

Enclosure-28-On January 4, 2006, the inspectors presented the integrated baseline inspection resultsto Paul Henninkamp, Vice President, Operations, and other members of licensee

management. The inspector confirmed that proprietary information was not provided or

examined during the inspection.ATTACHMENT: SUPPLEMENTAL INFORMATION

A-1AttachmentSUPPLEMENTAL INFORMATIONKEY POINTS OF CONTACTLicensee PersonnelM. Boyle, Manager, Radiation ProtectionD. Burnett, Superintendent, Chemistry

M. Cantrell, Operations Training Supervisor

J. Clark, Assistant Operations Manager - Training

T. Coleman, Manager, Planning and Scheduling/Outage

M. Davis, Acting Manager, Radiation Protection

C. Forpahl, Manager, Corrective Actions

H. Goodman, Director, Engineering

P. Hinnenkamp, Vice President - Operations

B. Houston, Manager, Plant Maintenance

G. Huston, Assistant Operations Manager - Shift

R. King, Director, Nuclear Safety Assurance

J. Leavines, Manager, Emergency Planning

D. Lorfing, Manager, Licensing

J. Maher, Superintendent, Reactor Engineering

W. Mashburn, Manager, Design Engineering

P. Russell, Manager, System Engineering

C. Stafford, Manager, Operations

W. Trudell, Manager, Training and Development

D. Vinci, General Manager - Plant OperationsLIST OF ITEMS OPENED, CLOSED, AND DISCUSSEDOpened and Closed05000458/2005005-01NCVInadequate procedure for implementation of an EAL05000458/2005005-02NCVFailure to complete TS required actions within allowedcompletion time05000458/2005005-03NCVInadequate design assumption results in RCIC turbineexhaust header filling with water following an automatichigh water level shutdownClosed05000458/2004-001-00LERAutomatic Reactor Scram Due to Main Generator TripResulting from Switchyard Fault

A-2AttachmentLIST OF DOCUMENTS REVIEWEDThe following documents were selected and reviewed by the inspectors to accomplish theobjectives and scope of the inspection and to support any findings:Section 1R11: Licensed Operator Requalification ProgramJob Performance MeasuresRJPM-OPS-052-04, Alternate Control Rod Drive Pumps, August 4, 2005RJPM-OPS-053-03R5, Reset a FCV runback, July 26, 2005

RJPM-OPS-109.4, July 26, 2005

RJPM-OPS-110-04, Synchronize the Main Generator with the Grid, August 2, 2005

RJPM-OPS-256-03R4, Restore level in the SBCT with deepwell pumps, July 26, 2005

RJPM-OPS-309-050, July 19, 2005

RJPM-OPS-508-04, Restore RPS B Normal Power Supply, August 19, 2005

RJPM-OPS-508-07, Respond to reactor scram with control rods failing to insert,August 2, 2005RJPM-OPS-800-17R1, Vent the CCRD over-piston volume, July 26, 2005RJPM-OPS-05206R2, Control rod operability faulted, July 12, 2005RJPM-OPS-05207R2, Alternate control rod drive pumps (Fuel Bldg), July 12, 2005

RJPM-OPS-05304R, Startup A recirc HPU, July 12, 2005

RJPM-OPS-20005R, Perform ATC actions for remote shutdown, August 2, 2005

RJPM-OPS-20006R5, Perform Attachment 13 UO actions, July 26, 2005

ScenariosRSMS-OPS-822, Loss of All Feed Water / RCIC Failure / LOCA, Revision: 00

RSMS-OPS-823, APRM Failure /SRV Failure / EHC Failure / ATWS, Revision: 00

RSMS-OPS-824, LPRM Failure / Loss of Vacuum with MSIV Closure / ATWS,Revision: 00

A-3AttachmentRSMS-OPS-825, Loss of RPS B / Relief Valve Fails Open / Steam Leak in the DrywellWith Failure of the Drywell, Revision: 00RSMS-OPS-827, Rod Drop / Fuel Failure / RCIC Steam Leak / Partial ATWS,Revision: 00RSMS-OPS-829, Failure Of STX-XS2B / Loss Of Condenser Vacuum / ATWS,Revision: 00RSMS-OPS-830, Inadvertent HPCS Injection and Loss of Stator Cooling, Revision: 00Section 1R17: Permanent Plant ModificationsEvent Notification 41252, Reactor Scram due to Loss of Vital Instrument BusLER 05-458/04-005-01, Unplanned Automatic Scram due to Loss of Non-Vital 120 VoltInstrument Bus, June 22, 2005CR-RBS-2004-04291 RCIC system initiated and subsequently tripped on Level 8CR-RBS-2005-00724 MR96-0063 removed internals from RCIC Turbine Exhaust CheckValve E51-VF040SDRP-P43, System Design Requirements Document, Reactor Core Isolation Cooling,Revision 0SDC-209, Reactor Core Isolation Cooling System Design Criteria, Revision 0,November 9, 1998SDC-209, Reactor Core Isolation Sooling System Design Criteria, Revision 3,September 27, 2004RBS USAR Section 5.4.6, Reactor Core Isolation Cooling System, Revision 17

NUREG-0989, RBS Safety Evaluation Report and Supplements, May 1984 throughOctober 1985GE SIL-30, HPCI/RCIC Turbine Exhaust Line Vacuum Breakers, October 31, 1973

GS AID-56, HPCI/RCI Turbine Exhaust Check Valve Cycling, August 1985

VPF-3622-353 (1) - 1, RCIC Turbine Instruction Manual, January 1975 throughMarch 1978MR96-0063, Remove Internals of [RCIC Exhaust Check Valve] E51-VF040,September 18, 1996

A-4AttachmentCR-RBS-1996-1671, Existing plant configuration of RCIC turbine exhaust line vacuumbreaker vent line does not correspond with configuration assumed in Calculation PH-56,

Revision 0Calculation PH-56, RCIC Turbine Exhaust Line Vacuum Breaker Vent Line SizingVerification, Revision 1A, November 27, 1996Piping and Instrument Drawing PID-27-06A, Reactor Core Isolation Cooling System,Revision 42Calculation G13.18.2.0-079, Determination of Quantity of Water Entering RCIC TurbineExhaust Line, May 11, 2005Calculation G13.18.10.2*225, RCIC Fluid Transient Analysis - Water in Turbine ExhaustLine, May 17, 2005ER-RB-2005-0084-000, Replace Check Valve E51-VF040 or Reinstall Internal Parts,February 20, 2005Terry Turbine SAM-12, Terry Wheel Water Slug Test, March 1, 1973Section 1EP2: Alert and Notification System TestingRiver Bend Station Emergency Plan, Revision 28River Bend Station Prompt Notification System Design Report, Revision 1,December 2001Section 1EP3: Emergency Response Organization Augmentation TestingEvaluation Reports for Pager and Augmentation Tests conducted:February 10, 2004June 17, 2004

August 24, 2004

September 23, 2004December 8, 2004January 25, 2005

March 22, 2005July 25, 2005September 27, 2005Section 1EP5: Correction of Emergency Preparedness Weaknesses and DeficienciesProceduresEN-LI-118, "Root Cause Analysis Process," Revision 1EN-LI-119, "Apparent Cause Evaluation Process," Revision 3

A-5AttachmentQuality AssuranceQuality Assurance Audit Report, QA-7-2003-RBS-1Quality Assurance Audit Report, QA-7-2004-RBS-1

Quality Assurance Audit Report, QA-7-2005-RBS-1Condition ReportsCR-RBS-1999-1316CR-RBS-2003-0586

CR-RBS-2003-0624

CR-RBS-2003-1950

CR-RBS-2003-1992

CR-RBS-2003-2094

CR-RBS-2003-3050

CR-RBS-2004-1090

CR-RBS-2004-1159CR-RBS-2004-3086CR-RBS-2004-3811

CR-RBS-2005-1433

CR-RBS-2005-1602

CR-RBS-2005-1632

CR-RBS-2005-1391

CR-RBS-2005-2516

CR-RBS-2005-2646Evaluation Reports for Drills conductedSeptember 3, 2003March 2 2004

April 20, 2004

May 25, 2004

June 9, 2004

July 27, 2004December 1, 2004 (simulator)December 1, 2004 (medical)

March 24, 2005

April 19, 2005

June 21, 2005Licensee Self-Assessments2004 Evaluated Exercise Pre-AssessmentLO-RLO-2004-00004 CA56, "2004 Long Range ERO Staffing Assessment"

2005 Emergency Planning Program Assessment

Snapshot Assessment of RBS Siren SystemSection 4OA1: Performance Indicator VerificationProceduresEN-EP-201, "Emergency Planning Performance Indicators," Revision 2EPP-2-703, "Performance Indicators," Revision 2

EIP-2-001, "Classification of Emergencies," Revision 12

EIP-2-002, "Classification Actions," Revision 24

EIP-2-006, "Notifications," Revision 32

EIP-2-007, "Protective Action Recommendation Guidelines," Revision 20

EIP-2-007, "Protective Action Recommendation Guidelines," Revision 21

A-6AttachmentSection 2OS2: ALARA Planning and ControlsCondition ReportsCR-RBS-2005-01472CR-RBS-2005-01474

CR-RBS-2005-02076CR-RBS-2005-02558CR-RBS-2005-03382

CR-RBS-2005-04004Audits and Self-AssessmentsQA-14-2005-RBS-1Quality Assurance Audit of Radiation Protection SnapshotAssessment /Benchmark on: Effectiveness of the RP TAC/TRG

(July 11-13, 2005)QS-2005-RBS-009ALARA Planning and Controls (August 22 throughSeptember 1, 2005)LO#2005-00123Radiation Protection Program (July 11-15, 2005)

Radiation Work Permits2005-1073Change out filter elements LWS-SKD5-F100A2005-1110Clean-up FB 113' cask pool and install cask pool impact limiter

2005-1310Recirc Flow Control Valve Maintenance ProceduresENS-RP-105Radiation Work Permits, Revision 7RP-110ALARA Program, Revision 2ALARA Committee MinutesAMC 05-01January 11, 2005AMC 05-02January 12, 2005

AMC 05-03January 17, 2005

AMC 05-11July 14, 2005Section 4OA2: Identification and Resolution of ProblemsCondition reportsCR-RBS-2005-02444CR-RBS-2005-02481

CR-RBS-2005-02486

CR-RBS-2005-02494

CR-RBS-2005-02548

CR-RBS-2005-02563CR-RBS-2005-02570CR-RBS-2005-02590

CR-RBS-2005-02605

CR-RBS-2005-02621

CR-RBS-2005-02624

CR-RBS-2005-02626

A-7AttachmentCR-RBS-2005-02645CR-RBS-2005-02649

CR-RBS-2005-02659

CR-RBS-2005-02664

CR-RBS-2005-02686

CR-RBS-2005-02693

CR-RBS-2005-02695

CR-RBS-2005-02722

CR-RBS-2005-02724

CR-RBS-2005-02727

CR-RBS-2005-02738

CR-RBS-2005-02754

CR-RBS-2005-02760

CR-RBS-2005-02767

CR-RBS-2005-02768

CR-RBS-2005-03106

CR-RBS-2005-03111

CR-RBS-2005-03114

CR-RBS-2005-03125

CR-RBS-2005-03131

CR-RBS-2005-03138

CR-RBS-2005-03151

CR-RBS-2005-03152

CR-RBS-2005-03165

CR-RBS-2005-03178

CR-RBS-2005-03182

CR-RBS-2005-03220

CR-RBS-2005-03242

CR-RBS-2005-03265

CR-RBS-2005-03273

CR-RBS-2005-03279

CR-RBS-2005-03443CR-RBS-2005-03446CR-RBS-2005-03471

CR-RBS-2005-03474

CR-RBS-2005-03503

CR-RBS-2005-03509

CR-RBS-2005-03513

CR-RBS-2005-03515

CR-RBS-2005-03554

CR-RBS-2005-03586

CR-RBS-2005-03594

CR-RBS-2005-03619

CR-RBS-2005-03629

CR-RBS-2005-03645

CR-RBS-2005-03670

CR-RBS-2005-03706

CR-RBS-2005-03728

CR-RBS-2005-03747

CR-RBS-2005-03753

CR-RBS-2005-03787

CR-RBS-2005-03831

CR-RBS-2005-03847

CR-RBS-2005-03887

CR-RBS-2005-03918

CR-RBS-2005-03948

CR-RBS-2005-03969

CR-RBS-2005-04018

CR-RBS-2005-04064

CR-RBS-2005-04071

CR-RBS-2005-04095

CR-RBS-2005-04103

CR-RBS-2005-04106

CR-RBS-2005-04118

A-8AttachmentLIST OF ACRONYMSALARAas low as is reasonably achievable

CFRCode of Federal RegulationsCRcondition report

CR-RBSRiver Bend Station condition report

EALemergency action level

FEMAFederal Emergency Management Agency

FCVflow control valve

HPUhydraulic power unit

MCmanual chapter

LERlicensee event report

LCOlimiting condition for operation

LOCAloss of coolant accident

NCVnoncited violation

NEINuclear Energy Institute

NRCU.S. Nuclear Regulatory Commission

RCICreactor core isolation cooling system

RCSreactor coolant system

RRreactor recirculation system

SOPsystem operating proceduresSTPsurveillance test procedure

TSTechnical Specification

USARUpdated Safety Analysis Report

WOwork order