IR 05000298/2014005: Difference between revisions
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| issue date = 02/11/2015 | | issue date = 02/11/2015 | ||
| title = IR 05000298/2014005; on 10/01/2014 - 12/31/2014; Cooper Nuclear Station; Follow-up of Events and Notices of Enforcement Discretion | | title = IR 05000298/2014005; on 10/01/2014 - 12/31/2014; Cooper Nuclear Station; Follow-up of Events and Notices of Enforcement Discretion | ||
| author name = Pruett T | | author name = Pruett T | ||
| author affiliation = NRC/RGN-IV/DRP | | author affiliation = NRC/RGN-IV/DRP | ||
| addressee name = Limpias O | | addressee name = Limpias O | ||
| addressee affiliation = Nebraska Public Power District (NPPD) | | addressee affiliation = Nebraska Public Power District (NPPD) | ||
| docket = 05000298 | | docket = 05000298 | ||
| license number = DPR-046 | | license number = DPR-046 | ||
| contact person = Groom J | | contact person = Groom J | ||
| case reference number = EA-14-219 | | case reference number = EA-14-219 | ||
| document report number = IR 2014005 | | document report number = IR 2014005 | ||
Line 19: | Line 19: | ||
=Text= | =Text= | ||
{{#Wiki_filter:UNITED STATES | {{#Wiki_filter:UNITED STATES ary 11, 2015 | ||
==SUBJECT:== | |||
COOPER NUCLEAR STATION - NRC INTEGRATED INSPECTION REPORT 05000298/2014005 AND EXERCISE OF ENFORCEMENT DISCRETION | |||
==Dear Mr. Limpias:== | ==Dear Mr. Limpias:== | ||
On December 31, 2014, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Cooper Nuclear Station. On January 15, 2015, the NRC inspectors | On December 31, 2014, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Cooper Nuclear Station. On January 15, 2015, the NRC inspectors discussed the results of this inspection with you and other members of your staff. Inspectors documented the results of this inspection in the enclosed inspection report. | ||
NRC inspectors documented one finding of very low safety significance (Green) in this report | NRC inspectors documented one finding of very low safety significance (Green) in this report. | ||
This finding involved a violation of NRC requirements. | |||
A violation involving the failure to maintain the operability of secondary containment during Operations with the Potential to Drain the Reactor Vessel (OPDRV) was identified. Specifically, from October 3, 2014, through October 22, 2014, Cooper Nuclear Station performed a total of 7 OPDRV activities with secondary containment inoperable in violation of Technical Specification 3.6.4.1, Secondary Containment. The NRC issued EGM 11-003, Enforcement Guidance Memorandum on Dispositioning Boiling Water Reactor Licensee Noncompliance with Technical Specification Containment Requirements During Operations with a Potential for Draining the Reactor Vessel, Revision 2, on December 13, 2013, allowing for the exercise of enforcement discretion for such OPDRV-related TS violations, when certain criteria are met. | |||
- | |||
The NRC concluded that Cooper Nuclear Station met these criteria. Therefore, I have been authorized, after consultation with the Director, Office of Enforcement to exercise enforcement discretion in accordance with Section 3.5, Violations Involving Special Circumstances, of the NRC Enforcement Policy and, therefore, will not issue enforcement action for this violation, subject to a timely license amendment request being submitted. | |||
If you contest the violation or significance of the non-cited violation, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC resident inspector at the Cooper Nuclear Station. If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region IV; and the NRC resident inspector at the Cooper Nuclear Station. | |||
ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading | In accordance with Title 10 of the Code of Federal Regulations (10 CFR) 2.390, Public Inspections, Exemptions, Requests for Withholding, a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRCs Public Document Room or from the Publicly Available Records (PARS) component of the NRC's Agencywide Documents Access and Management System (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room). | ||
-rm/adams.html (the Public Electronic Reading Room). | |||
Sincerely, | Sincerely, | ||
/RA T. Farnholtz for/ | /RA T. Farnholtz for/ | ||
Troy Pruett Director Division of Reactor Projects Docket Nos. | Troy Pruett Director Division of Reactor Projects Docket Nos. 50-298 License Nos. DPR-46 | ||
===Enclosure:=== | |||
Inspection Report 05000298/2014005 w/ Attachments: | |||
1. Supplemental Information 2. Request for Information for the O | |||
REGION IV== | |||
Docket: 05000298 License: DPR-46 Report: 05000298/2014005 Licensee: Nebraska Public Power District Facility: Cooper Nuclear Station Location: 72676 648A Ave Brownville, NE Dates: October 1, 2014 through December 31, 2014 Inspectors: J. Josey, Senior Resident Inspector E. Coffman, Acting Senior Resident Inspector C. Henderson, Resident Inspector R. Azua, Senior Project Engineer M. Langelier, Project Engineer L. Carson II, Senior Health Physicist P. Hernandez, Health Physicist J. Drake, Senior Reactor Inspector P. Elkmann, Senior Emergency Preparedness Inspector Approved Jeremy Groom By: Acting Chief, Project Branch C Division of Reactor Projects-1- Enclosure | |||
J. Josey, Senior Resident Inspector E. Coffman, Acting Senior Resident Inspector C. Henderson, Resident Inspector R. Azua, Senior Project Engineer M. Langelier, Project Engineer L. Carson II , Senior Health Physicist P. Hernandez, Health Physicist J. Drake, Senior Reactor Inspector P. Elkmann, Senior Emergency Preparedness Inspector Approved By: | |||
=SUMMARY= | =SUMMARY= | ||
IR | IR 05000298/2014005; 10/01/2014 - 12/31/2014; Cooper Nuclear Station; Follow-up of Events and Notices of Enforcement Discretion. | ||
The inspection activities described in this report were performed between October 1 and December 31, 2014, by the resident inspectors at the Cooper Nuclear Station and inspectors from the NRCs Region IV office. One finding of very low safety significance (Green) was documented in this report. This finding involved a violation of NRC requirements. The significance of inspection findings is indicated by their color (Green, White, Yellow, or Red), | |||
which is determined using Inspection Manual Chapter 0609, Significance Determination Process. Their cross-cutting aspects are determined using Inspection Manual Chapter 0310, | |||
Aspects within the Cross-Cutting Areas. Violations of NRC requirements are dispositioned in accordance with the NRC Enforcement Policy. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process. | |||
The inspection activities described in this report were performed between October 1 and December 31, 2014, by the resident inspectors at the Cooper Nuclear Station and inspectors from the | |||
The | |||
-1649, | |||
===Cornerstone: Barrier Integrity=== | ===Cornerstone: Barrier Integrity=== | ||
: '''Green.''' | : '''Green.''' | ||
The inspectors reviewed a self-revealing, non-cited violation of 10 CFR Part 50, Appendix B, Criterion V, | The inspectors reviewed a self-revealing, non-cited violation of 10 CFR Part 50, | ||
-2/D-100 Modified REM*TAKE 2, | Appendix B, Criterion V, Instructions, Procedures, and Drawings, associated with the licensees failure to follow Special Procedure GEH-TP-116, Procedure for the Operation and Maintenance of the REM*TAKE-2/D-100 Modified REM*TAKE 2, Revision 3, for post-maintenance testing following corrective maintenance. Specifically, the licensee did not follow post-maintenance testing requirements associated with the calibration of the bleeder valve for the REM*TAKE-2/D-100 tool following corrective maintenance to address water intrusion. This resulted in the bleeder valve being misadjusted and nullifying the fail-safe feature of the REM*TAKE-2/D-100 tool. With the fail-safe nullified, Control Rod Blade 30-47 became disengaged from the REM*TAKE-2/D-100 tool and dropped onto the reactor core top guide when the supplemental employee inadvertently pressed the disengage button. No reactor fuel was damaged as indicated by normal radiation levels and air samples on the refuel floor and reactor water coolant samples. The licensees immediate corrective actions for the event was to suspended all in-vessel maintenance activities and remove REM*Take-2/D-100 grapple from service and determined functionality of the tool. The licensee entered this deficiency into their corrective action program for resolution as Condition Report CR-CNS-2014-06809. | ||
-2/D-100 tool following corrective maintenance to address water intrusion. This resulted in the bleeder valve being misadjusted and nullifying the fail-safe feature of the REM*TAKE | |||
-2/D-100 tool. With the fail-safe nullified | |||
, Control Rod Blade 30-47 became disengaged from the REM*TAKE | |||
-2/D-100 tool and dropped onto the reactor core top guide when the supplemental employee inadvertently pressed the disengage button. No reactor fuel was damaged as indicated by normal radiation levels and air samples on the refuel floor and reactor water coolant samples. The | |||
The finding has a cross-cutting aspect in the area of human performance associated with the field presence component because the licensee failed to ensure supervisory and management oversight of work activities including contractors and supplemental personnel | The licensees failure to follow the post-maintenance testing requirements in Special Procedure GEH-TP-116 was a performance deficiency. The performance deficiency was more than minor, and therefore a finding, because it was associated with the human performance attribute of the Barrier Integrity Cornerstone and affected the associated objective of maintaining functionality of fuel cladding. Specifically, with the fail-safe nullified, | ||
Control Rod Blade 30-47 became disengaged from the REM*TAKE-2/D-100 tool and dropped onto the reactor core top guide when a supplemental employee inadvertently pressed the disengage button. Using Inspection Manual Chapter 0609, Appendix G, | |||
Attachment 1, Shutdown Operations Significance Determination Process Phase 1 Initial Screening and Characterization of Findings, dated May 09, 2014, inspectors determined that the finding was of very low safety significance (Green) because the finding did not impact the fuel barrier because it: (1) does not increase the potential for failure of the freeze seal or if unmitigated have the potential to cause a disruption of residual heat removal/decay heat removal or a loss of inventory event; (2) does not involve two or more adjacent control rods with the potential to, or actually, add postive reactivity; and (3) does not degrade the ability to isolate a drain down or leakage path. The finding has a cross-cutting aspect in the area of human performance associated with the field presence component because the licensee failed to ensure supervisory and management oversight of work activities including contractors and supplemental personnel [H.2]. (Section 4OA3) | |||
=PLANT STATUS= | =PLANT STATUS= | ||
The Cooper Nuclear Station began the inspection period shutdown for Refueling Outage 28 , which began on September 27, 2014 , during the previous quarter. On November 1, 2014 , the station | The Cooper Nuclear Station began the inspection period shutdown for Refueling Outage 28, which began on September 27, 2014, during the previous quarter. On November 1, 2014, the station commenced reactor startup and the reactor was critical. On November 2, 2014, the station synchronized the main generator with the grid and began power ascension. The plant returned to full power on November 5, 2014, where it remained for the rest of the reporting period. | ||
REPORT DETAILS | |||
==REACTOR SAFETY== | ==REACTOR SAFETY== | ||
Cornerstones: | Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity {{a|1R04}} | ||
==1R04 Equipment Alignment== | |||
{{IP sample|IP=IP 71111.04}} | |||
Partial Walkdown | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors performed partial system walk | The inspectors performed partial system walk-downs of the following risk-significant systems: | ||
-downs of the following risk | * October 15, 2014, Residual heat removal shutdown cooling, Loop A | ||
-significant systems: | * November 5, 2014, Residual heat removal A low-pressure coolant injection during unplanned limiting condition for operation for residual heat removal B low-pressure coolant injection | ||
* November 10, 2014, Standby gas treatment A The inspectors reviewed the licensees procedures and system design information to determine the correct lineup for the systems. They visually verified that critical portions of the systems were correctly aligned for the existing plant configuration. | |||
-down samples as defined | |||
These activities constituted three partial system walk-down samples as defined in Inspection Procedure 71111.04. | |||
====b. Findings==== | ====b. Findings==== | ||
No findings were identified. | No findings were identified. {{a|1R05}} | ||
==1R05 Fire Protection== | |||
{{IP sample|IP=IP 71111.05}} | |||
===.1 Quarterly Inspection=== | ===.1 Quarterly Inspection=== | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors evaluated the | The inspectors evaluated the licensees fire protection program for operational status and material condition. The inspectors focused their inspection on four plant areas important to safety: | ||
: | * October 4, 2014, Residual heat removal pump room, Fire Area I, Zone 1C | ||
October 4, 2014, Residual heat removal pump room, Fire Area I, Zone 1C | * October 8, 2014, Fire impairment for BLDG-DOOR-R209 and R208, Fire Area II, Zone 3A and Fire Area III, Zone 3B | ||
-DOOR-R209 and R208, Fire Area II, Zone 3A and Fire Area III, Zone 3B | * December 8, 2014, Battery room 1A, Fire Area IV(A), Zone 8E | ||
* December 8, 2014, DC switchgear room 1A, Fire Area IV(A), Zone 8H For each area, the inspectors evaluated the fire plan against defined hazards and defense-in-depth features in the licensees fire protection program. The inspectors evaluated control of transient combustibles and ignition sources, fire detection and suppression systems, manual firefighting equipment and capability, passive fire protection features, and compensatory measures for degraded conditions. | |||
protection features, and compensatory measures for degraded conditions. | |||
These activities | These activities constituted four quarterly inspection samples, as defined in Inspection Procedure 71111.05. | ||
====b. Findings==== | ====b. Findings==== | ||
Line 150: | Line 107: | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
On November 21, 2014, the inspectors completed their annual evaluation of the | On November 21, 2014, the inspectors completed their annual evaluation of the licensees fire brigade performance. This evaluation included observation of an announced fire drill for the non-critical switchroom. During this drill, the inspectors evaluated the capability of the fire brigade members, the leadership ability of the brigade leader, the brigades use of turnout gear and fire-fighting equipment, and the effectiveness of the fire brigades team operation. The inspectors also reviewed whether the licensees fire brigade met NRC requirements for training, dedicated size and membership, and equipment. | ||
. During this drill, the inspectors evaluated the capability of the fire brigade members, the leadership ability of the brigade leader, the | |||
-fighting equipment, and the effectiveness of the fire | |||
These activities | These activities constituted one annual inspection sample, as defined in Inspection Procedure 71111.05. | ||
====b. Findings==== | ====b. Findings==== | ||
No findings were identified. | No findings were identified. {{a|1R07}} | ||
==1R07 Heat Sink Performance== | |||
{{IP sample|IP=IP 71111.07}} | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
On November 17, 2014 , the inspectors completed an inspection of the readiness and availability of risk | On November 17, 2014, the inspectors completed an inspection of the readiness and availability of risk-significant heat exchangers. The inspectors observed performance testing, reviewed the data from the performance test, and verified the licensee used the industry standard periodic maintenance method outlined in EPRI NP-7552 for the B reactor equipment cooling heat exchanger. Additionally, the inspectors walked down the heat exchanger to observe its performance and material condition and verified that the heat exchanger was correctly categorized under the Maintenance Rule and was receiving the required maintenance. | ||
-significant heat exchangers. The inspectors observed performance testing, reviewed the data from the performance test, | |||
-7552 for | |||
These activities constitute completion of one heat sink performance annual review sample , as defined in Inspection Procedure 71111.07. | These activities constitute completion of one heat sink performance annual review sample, as defined in Inspection Procedure 71111.07. | ||
====b. Findings==== | ====b. Findings==== | ||
No findings were identified. | No findings were identified. {{a|1R08}} | ||
==1R08 Inservice Inspection Activities== | |||
{{IP sample|IP=IP 71111.08}} | |||
===.1 Non-destructive Examination (NDE) Activities and Welding Activities=== | ===.1 Non-destructive Examination (NDE) Activities and Welding Activities=== | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors directly observed the following nondestructive examinations: | The inspectors directly observed the following nondestructive examinations: | ||
SYSTEM WELD IDENTIFICATION EXAMINATION TYPE | SYSTEM WELD IDENTIFICATION EXAMINATION TYPE Main Steam MSH-152 Visual Reactor Vessel HME-88-3 Ultrasonic Reactor Vessel VC8-8C-6 Magnetic Particle The inspectors reviewed records for the following nondestructive examinations: | ||
SYSTEM WELD IDENTIFICATION EXAMINATION TYPE Main Steam VR-DA-2 Visual Main Steam MS-S8 Visual Reactor Pressure | SYSTEM WELD IDENTIFICATION EXAMINATION TYPE Main Steam VR-DA-2 Visual Main Steam MS-S8 Visual Reactor Pressure PRE-BG1-1 Ultrasonic Vessel Reactor Pressure PRE-BG1-26 Ultrasonic Vessel Control Rod Drive CRD-26-51-1 Dye Penetrant Control Rod Drive CRD-26-03-1 Dye Penetrant Control Rod Drive CRD-30-03-1 Dye Penetrant During the review and observation of each examination, the inspectors observed whether activities were performed in accordance with the ASME Code requirements and applicable procedures. The inspectors also reviewed the qualifications of all nondestructive examination technicians performing the inspections to determine whether they were current. | ||
The inspectors directly observed a portion of the following welding activities: | The inspectors directly observed a portion of the following welding activities: | ||
SYSTEM WELD IDENTIFICATION EXAMINATION TYPE | SYSTEM WELD IDENTIFICATION EXAMINATION TYPE Service Water FW-8 Shielded Metal Arc Welding Service Water FW-9 Shielded Metal Arc Welding Reactor Water RWCU-CV-15 FW-8 Gas Tungsten Arc Cleanup Welding The inspectors reviewed records for the following welding activities: | ||
SYSTEM WELD IDENTIFICATION EXAMINATION TYPE | SYSTEM WELD IDENTIFICATION EXAMINATION TYPE Service Water FW-10 Shielded Metal Arc Welding Service Water FW-11 Shielded Metal Arc Welding The inspectors reviewed whether the welding procedure specifications and the welders had been properly qualified in accordance with ASME Code Section IX requirements. | ||
The inspectors also determined whether essential variables were identified, recorded in the procedure qualification record, and formed the bases for qualification of the welding procedure specifications. | |||
These activities constitute completion of one inservice inspection sample, as defined in Inspection Procedure 71111.08. | These activities constitute completion of one inservice inspection sample, as defined in Inspection Procedure 71111.08. | ||
Line 187: | Line 143: | ||
No findings were identified. | No findings were identified. | ||
===.2 | ===.2 Identification and Resolution of Problems=== | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors reviewed 23 condition reports which dealt with inservice inspection activities and found the corrective actions for inservice inspection issues were appropriate. The specific condition reports reviewed are listed in the documents reviewed section. From this review, the inspectors concluded that the licensee has an appropriate threshold for entering inservice inspection issues into the corrective action program and has procedures that direct a root cause evaluation when necessary. The licensee also has an effective program for applying industry inservice inspection | The inspectors reviewed 23 condition reports which dealt with inservice inspection activities and found the corrective actions for inservice inspection issues were appropriate. The specific condition reports reviewed are listed in the documents reviewed section. From this review, the inspectors concluded that the licensee has an appropriate threshold for entering inservice inspection issues into the corrective action program and has procedures that direct a root cause evaluation when necessary. The licensee also has an effective program for applying industry inservice inspection operating experience. Specific documents reviewed during this inspection are listed in the attachment. | ||
These actions constitute completion of the requirements of Section 02.05. | |||
====b. Findings==== | ====b. Findings==== | ||
No findings were identified. {{a|1R11}} | |||
==1R11 Licensed Operator Requalification Program and Licensed Operator Performance== | |||
{{IP sample|IP=IP 71111.11}} | |||
===.1 Review of Licensed Operator Requalification=== | ===.1 Review of Licensed Operator Requalification=== | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
On November 19, 2014, the inspectors observed an evaluated simulator scenario performed by an operating crew. The inspectors assessed the performance of the operators and the evaluators | On November 19, 2014, the inspectors observed an evaluated simulator scenario performed by an operating crew. The inspectors assessed the performance of the operators and the evaluators critique of their performance. The inspectors also assessed the modeling and performance of the simulator during the requalification activities. | ||
These activities constitute completion of one quarterly licensed operator requalification program sample, as defined in Inspection Procedure 71111.11. | |||
====b. Findings==== | ====b. Findings==== | ||
Line 206: | Line 167: | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
On November 1, 2014, the inspectors observed the performance of on | On November 1, 2014, the inspectors observed the performance of on-shift licensed operators in the plants main control room. At the time of the observations, the plant was in a period of heightened activity and risk due to reactor startup. | ||
-shift licensed operators in the | |||
These activities constitute completion of one quarterly licensed operator performance sample , | In addition, the inspectors assessed the operators adherence to plant procedures, including conduct of operations procedure, and other operations department policies. | ||
These activities constitute completion of one quarterly licensed operator performance sample, as defined in Inspection Procedure 71111.11. | |||
====b. Findings==== | ====b. Findings==== | ||
No findings were identified. | No findings were identified. {{a|1R12}} | ||
==1R12 Maintenance Effectiveness== | |||
{{IP sample|IP=IP 71111.12}} | |||
====a. Inspection Scope==== | |||
The inspectors reviewed two instances of degraded performance or condition of safety-related structures, systems, and components (SSCs): | |||
* November 5, 2014, Reactor equipment cooling heat exchanger B | |||
* December 16, 2014, 125 VDC charger 1A The inspectors reviewed the extent of condition of possible common cause structure, system, and component failures and evaluated the adequacy of the licensees corrective actions. The inspectors reviewed the licensees work practices to evaluate whether these may have played a role in the degradation of the structure, system, or component. | |||
The inspectors assessed the licensees characterization of the degradation in accordance with 10 CFR 50.65 (the Maintenance Rule), and verified that the licensee was appropriately tracking degraded performance and conditions in accordance with the Maintenance Rule. | |||
These activities | These activities constituted completion of two maintenance effectiveness samples, as defined in Inspection Procedure 71111.12. | ||
====b. Findings==== | ====b. Findings==== | ||
No findings were identified. | No findings were identified. {{a|1R13}} | ||
==1R13 Maintenance Risk Assessments and Emergent Work Control== | |||
{{IP sample|IP=IP 71111.13}} | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors reviewed four risk assessments performed by the licensee prior to changes in plant configuration and the risk management actions taken by the licensee in response to elevated risk: | The inspectors reviewed four risk assessments performed by the licensee prior to changes in plant configuration and the risk management actions taken by the licensee in response to elevated risk: | ||
October 20, 2014, 4160 | * October 20, 2014, 4160 VAC, Bus G outage | ||
-AOV-TCV451B unavailable November 24, 2014, Temporary fans associated with alternate decay heat removal room The inspectors verified that these risk | * November 1, 2014, Dredging in the area of the intake structure barrage impact | ||
* November 4, 2014, Technical Specification Limiting Condition for Operation 3.0.4.b risk evaluation, Mode 1 and 2 entry with SW-AOV-TCV451B unavailable | |||
* November 24, 2014, Temporary fans associated with alternate decay heat removal room The inspectors verified that these risk assessments were performed timely and in accordance with the requirements of 10 CFR 50.65 (the Maintenance Rule) and plant procedures. The inspectors reviewed the accuracy and completeness of the licensees risk assessments and verified that the licensee implemented appropriate risk management actions based on the result of the assessments. | |||
The inspectors also observed portions of two emergent work activities that had the potential to affect the functional capability of mitigating systems | The inspectors also observed portions of two emergent work activities that had the potential to affect the functional capability of mitigating systems. | ||
. | * November 12, 2014, Residual heat removal injection valve RHR-MOV-27B failing to open | ||
* November 12, 2014, Diesel generator 2, 3R cylinder injector pump replacement The inspectors verified that the licensee appropriately developed and followed a work plan for these activities. The inspectors verified that the licensee took precautions to minimize the impact of the work activities on unaffected structures, systems, and components (SSCs). | |||
These activities constitute completion of six maintenance risk assessments and emergent work control inspection samples, as defined in Inspection Procedure 71111.13. | |||
These activities constitute completion of six maintenance risk assessments and emergent work control inspection samples , as defined in Inspection Procedure 71111.13. | |||
====b. Findings==== | ====b. Findings==== | ||
No findings were identified. | No findings were identified. {{a|1R15}} | ||
==1R15 Operability Determinations and Functionality Assessments== | |||
{{IP sample|IP=IP 71111.15}} | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors reviewed four operability determinations and functionality assessments that the licensee performed for degraded or nonconforming structures, systems, or components (SSCs): | The inspectors reviewed four operability determinations and functionality assessments that the licensee performed for degraded or nonconforming structures, systems, or components (SSCs): | ||
November 18, 2014 , CR-CNS- | * November 18, 2014, CR-CNS-2014-06602, Operability determination of 480 VAC, Bus G, anchor bolts | ||
-CNS-2014-07978, Operability determination of Division I service water system SW | * November 18, 2014, CR-CNS-2014-07552 and CR-CNS-2014-07978, Operability determination of Division I service water system SW-V-108 failed to open during post-loss of coolant accident flow to control room air conditioner | ||
-V-108 failed to open during post | * November 19, 2014, Operability determination of secondary containment with railroad inner airlock door open | ||
-loss of coolant accident flow to control room air conditioner November 19, 2014, Operability determination of | * December 15, 2014, CR-CNS-2014-08280 and CR-CNS-2014-08316, Functionality assessment of reactor core isolation cooling steam leak on drip leg trap inlet The inspectors reviewed the timeliness and technical adequacy of the licensees evaluations. Where the licensee determined the degraded structure, system, or component to be operable or functional, the inspectors verified that the licensees compensatory measures were appropriate to provide reasonable assurance of operability or functionality. The inspectors verified that the licensee had considered the effect of other degraded conditions on the operability or functionality of the degraded structure, system, or component. | ||
-CNS-2014-08316 , Functionality assessment of reactor core isolation cooling steam leak on drip leg trap inlet The inspectors reviewed the timeliness and technical adequacy of the | |||
These activities constitute completion of four operability and functionality review samples, as defined in Inspection Procedure 71111.15. | |||
====b. Findings==== | ====b. Findings==== | ||
No findings were identified. | No findings were identified. {{a|1R18}} | ||
==1R18 Plant Modifications== | |||
{{IP sample|IP=IP 71111.18}} | |||
====a. Inspection Scope==== | |||
The inspectors reviewed two permanent plant modifications that affected risk-significant structures, systems, and components (SSCs): | |||
* October 7, 2014, modification to address 125 VDC battery rack B non-conforming bolting configuration | |||
* October 27, 2014, HPCI-MO-14 valve replacement change evaluation document 6017820 The inspectors reviewed the design and implementation of the modifications. The inspectors verified that work activities involved in implementing the modifications did not adversely impact operator actions that may be required in response to an emergency or other unplanned event. The inspectors verified that post-modification testing was adequate to establish the operability of the structures, systems, and components as modified. | |||
These activities constitute completion of two samples of permanent modifications, as defined in Inspection Procedure 71111.18. | |||
====b. Findings==== | ====b. Findings==== | ||
No findings were identified. | No findings were identified. {{a|1R19}} | ||
==1R19 Post-Maintenance Testing== | |||
{{IP sample|IP=IP 71111.19}} | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors reviewed six post-maintenance testing activities that affected risk | The inspectors reviewed six post-maintenance testing activities that affected risk-significant structures, systems, or components (SSCs): | ||
-significant structures, systems, or components (SSCs): | * October 21, 2014, Z sump pump Z1 high high level switch replacement | ||
October 21, 2014, Z sump pump Z1 high high level switch replacement October 22, 2014, Diesel generator 2 fuel oil injection pumps replacement October 27, 2014, Main steam isolation valve 80A, 80D, 86A, and 86D air operated and manifold maintenance November 4, 2014, 125/250 | * October 22, 2014, Diesel generator 2 fuel oil injection pumps replacement | ||
-MOV-14 replacement The inspectors reviewed licensing and design | * October 27, 2014, Main steam isolation valve 80A, 80D, 86A, and 86D air operated and manifold maintenance | ||
-basis documents for the structures, systems, and | * November 4, 2014, 125/250 VDC B battery replacement | ||
* November 4, 2014, Diesel generator 1 6-year inspection and maintenance | |||
* November 4, 2014, HPCI-MOV-14 replacement The inspectors reviewed licensing and design-basis documents for the structures, systems, and components, and the maintenance and post-maintenance test procedures. | |||
The inspectors observed the performance of the post | The inspectors observed the performance of the post-maintenance tests to verify that the licensee performed the tests in accordance with approved procedures, satisfied the established acceptance criteria, and restored the operability of the affected structures, systems, and components. | ||
-maintenance tests to verify that the licensee performed the tests in accordance with approved procedures, satisfied the established acceptance criteria, and restored the operability of the affected structures, systems, and | |||
These activities constitute completion of six post-maintenance testing inspection samples , as defined in Inspection Procedure 71111.19. | These activities constitute completion of six post-maintenance testing inspection samples, as defined in Inspection Procedure 71111.19. | ||
====b. Findings==== | ====b. Findings==== | ||
No findings were identified. | No findings were identified. {{a|1R20}} | ||
==1R20 Refueling and Other Outage Activities== | |||
{{IP sample|IP=IP 71111.20}} | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
During | During the stations refueling outage that concluded on November 2, 2014, the inspectors evaluated the licensees outage activities. The inspectors verified that the licensee considered risk in developing and implementing the outage plan, appropriately managed personnel fatigue, and developed mitigation strategies for losses of key safety functions. This verification included the following: | ||
Review of the | * Review of the licensees outage plan prior to the outage | ||
-down and cool | * Monitoring of shut-down and cool-down activities | ||
-down activities Verification that the licensee maintained defense | * Verification that the licensee maintained defense-in-depth during outage activities | ||
-in-depth during outage activities Observation and review of operations with a potential for draining the reactor vessel | * Observation and review of operations with a potential for draining the reactor vessel | ||
-up and startup activities These activities constitute completion of one refueling outage sample , | * Observation and review of fuel handling activities | ||
* Monitoring of heat-up and startup activities These activities constitute completion of one refueling outage sample, as defined in Inspection Procedure 71111.20. | |||
====b. Findings==== | ====b. Findings==== | ||
No findings were identified. | No findings were identified. {{a|1R22}} | ||
==1R22 Surveillance Testing== | |||
{{IP sample|IP=IP 71111.22}} | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors observed five risk-significant surveillance tests and reviewed test results to verify that these tests adequately demonstrated that the structures, systems, and components (SSCs) were capable of performing their safety functions: | The inspectors observed five risk-significant surveillance tests and reviewed test results to verify that these tests adequately demonstrated that the structures, systems, and components (SSCs) were capable of performing their safety functions: | ||
In-service | In-service tests: | ||
-AO-740 and RR-AO-741 operability and closure timing test Other surveillance tests: | * November 4, 2014, High pressure coolant injection Containment isolation valve surveillance tests: | ||
October 27, 2014, Reactor core isolation coolant local leak rate test RWCU-15CV, RCIC-MOV-15, and RCIC | * October 6, 2014, Primary containment isolation valves RR-AO-740 and RR-AO-741 operability and closure timing test Other surveillance tests: | ||
-MOV-16 | * October 27, 2014, Reactor core isolation coolant local leak rate test RWCU-15CV, RCIC-MOV-15, and RCIC-MOV-16 | ||
-rate test | * November 1, 2014, Main steam line isolation valve local leak rate testing | ||
* November 3, 2014, Control rod drive hatch local leak-rate test The inspectors verified that these tests met technical specification requirements, that the licensee performed the tests in accordance with their procedures, and that the results of the test satisfied appropriate acceptance criteria. The inspectors verified that the licensee restored the operability of the affected structures, systems, and components following testing. | |||
These activities constitute completion of five surveillance testing inspection samples , | These activities constitute completion of five surveillance testing inspection samples, as defined in Inspection Procedure 71111.22. | ||
====b. Findings==== | ====b. Findings==== | ||
No findings were identified. | No findings were identified. | ||
===Cornerstone: | ===Cornerstone: Emergency Preparedness=== | ||
{{a|1EP4}} | |||
==1EP4 Emergency Action Level and Emergency Plan Changes== | |||
{{IP sample|IP=IP 71114.04}} | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspector performed an in | The inspector performed an in-office review of the Cooper Nuclear Station Emergency Plan, Revision 65, dated June 23, 2014. This revision: | ||
-office review of the Cooper Nuclear Station Emergency Plan, Revision 65, dated June 23, 2014. This revision: | * Defined hostile action | ||
-0654, | * Added detail about the process for requesting offsite assistance for fire fighting | ||
-generated changes; therefore, this revision is subject to future inspection. | * Added detail about the telephone connectivity between the licensees site and its Emergency Operations Facility | ||
* Added detail about the radio communications systems available to the Operations and Security departments during an emergency | |||
* Added a requirement to maintain satellite phones in the licensees Control Room, Technical Support Center, Emergency Operations Facility, and Joint Information Center | |||
* Added a requirement to maintain informational signs for the public using the Steamboat Trace Trail | |||
* Deleted a requirement to maintain respiratory protection equipment (self-contained breathing apparatus) at the Communications Building | |||
* Deleted references to the use of the Auburn Rescue Squad and Nemaha County Hospital Rescue Squad in transporting injured station personnel to medical facilities | |||
* Corrected typographical errors and titles, and made other administrative changes This revision was compared to its previous revision, to the criteria of NUREG-0654, Criteria for Preparation and Evaluation of Radiological Emergency Response Plans and Preparedness in Support of Nuclear Power Plants, Revision 1, and to the standards in 10 CFR 50.47(b) to determine if the revision adequately implemented the requirements of 10 CFR 50.54(q)(3) and 50.54(q)(4). The inspector verified that the revision did not decrease the effectiveness of the emergency plan. This review was not documented in a safety evaluation report and did not constitute approval of licensee-generated changes; therefore, this revision is subject to future inspection. | |||
These activities constitute completion of one emergency action level and emergency plan changes sample as defined in Inspection Procedure 71114.04. | These activities constitute completion of one emergency action level and emergency plan changes sample as defined in Inspection Procedure 71114.04. | ||
Line 334: | Line 305: | ||
==RADIATION SAFETY== | ==RADIATION SAFETY== | ||
Cornerstones: | Cornerstones: Public Radiation Safety and Occupational Radiation Safety {{a|2RS1}} | ||
Public Radiation Safety and Occupational Radiation Safety | ==2RS1 Radiological Hazard Assessment and Exposure Controls== | ||
{{IP sample|IP=IP 71124.01}} | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors assessed the | The inspectors assessed the licensees performance in assessing the radiological hazards in the workplace associated with licensed activities. The inspectors assessed the licensees implementation of appropriate radiation monitoring and exposure control measures for both individual and collective exposures. The inspectors walked down various portions of the plant and performed independent radiation dose rate measurements. The inspectors interviewed the radiation protection manager, radiation protection supervisors, and radiation workers. The inspectors reviewed licensee performance in the following areas: | ||
The hazard assessment program, including a review of the | * The hazard assessment program, including a review of the licensees evaluations of changes in plant operations and radiological surveys to detect dose rates, airborne radioactivity, and surface contamination levels | ||
-assessments, and corrective action documents related to radiological hazard assessment and exposure controls since the last inspection These activities constitute completion of one sample of radiological hazard assessment and exposure controls as defined in Inspection Procedure 71124.01. | * Instructions and notices to workers, including labeling or marking containers of radioactive material, radiation work permits, actions for electronic dosimeter alarms, and changes to radiological conditions | ||
* Programs and processes for control of sealed sources and release of potentially contaminated material from the radiologically controlled area, including survey performance, instrument sensitivity, release criteria, procedural guidance, and sealed source accountability | |||
* Radiological hazards control and work coverage, including the adequacy of surveys, radiation protection job coverage and contamination controls, the use of electronic dosimeters in high noise areas, dosimetry placement, airborne radioactivity monitoring, controls for highly activated or contaminated materials (non-fuel) stored within spent fuel and other storage pools, and posting and physical controls for high radiation areas and very high radiation areas | |||
* Radiation worker and radiation protection technician performance with respect to radiation protection work requirements | |||
* Audits, self-assessments, and corrective action documents related to radiological hazard assessment and exposure controls since the last inspection These activities constitute completion of one sample of radiological hazard assessment and exposure controls as defined in Inspection Procedure 71124.01. | |||
====b. Findings==== | ====b. Findings==== | ||
No findings were identified. | No findings were identified. {{a|2RS3}} | ||
==2RS3 In-Plant Airborne Radioactivity Control and Mitigation== | |||
{{IP sample|IP=IP 71124.03}} | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors evaluated whether the licensee controlled in | The inspectors evaluated whether the licensee controlled in-plant airborne radioactivity concentrations consistent with ALARA principles and that the use of respiratory protection devices did not pose an undue risk to the wearer. During the inspection, the inspectors interviewed licensee personnel, walked down various portions of the plant, and reviewed licensee performance in the following areas: | ||
-plant airborne radioactivity concentrations consistent with ALARA principles and that the use of respiratory protection devices did not pose an undue risk to the wearer. During the inspection, the inspectors interviewed licensee personnel, walked down various portions of the plant, and reviewed licensee performance in the following areas: | * The licensees use, when applicable, of ventilation systems as part of its engineering controls | ||
The | * The licensees respiratory protection program for use, storage, maintenance, and quality assurance of National Institute for Occupational Safety and Health (NIOSH)-certified equipment, qualification and training of personnel, and user performance | ||
-assessments, and corrective action documents related to in-plant airborne radioactivity control and mitigation since the last inspection These activities constitute completion of one sample of in-plant airborne radioactivity control and mitigation as defined in Inspection Procedure 71124.03. | * The licensees capability for refilling and transporting self-contained breathing apparatus (SCBA) air bottles to and from the control room and operations support center during emergency conditions, status of self-contained breathing apparatus staged and ready for use in the plant and associated surveillance records, and personnel qualification and training | ||
* Audits, self-assessments, and corrective action documents related to in-plant airborne radioactivity control and mitigation since the last inspection These activities constitute completion of one sample of in-plant airborne radioactivity control and mitigation as defined in Inspection Procedure 71124.03. | |||
====b. Findings==== | ====b. Findings==== | ||
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==OTHER ACTIVITIES== | ==OTHER ACTIVITIES== | ||
Cornerstones: | Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Security | ||
{{a|4OA1}} | |||
==4OA1 Performance Indicator Verification== | |||
{{IP sample|IP=IP 71151}} | |||
===.1 Mitigating System Performance Index: Emergency AC Power Systems (MS06), High=== | |||
Pressure Injection Systems (MS07), Heat Removal Systems (MS08), Residual Heat Removal Systems (MS09), and Cooling Water Systems (MS10) | |||
====a. Inspection Scope==== | |||
The inspectors reviewed the licensees mitigating system performance index data for the period of September 22, 2013 through September 30, 2014, to verify the accuracy and completeness of the reported data. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, to determine the accuracy of the reported data. | |||
These activities constituted verification of the mitigating system performance index for emergency ac power systems, high pressure injection systems, heat removal systems, residual heat removal systems, and cooling water systems, as defined in Inspection Procedure 71151. | |||
====b. Findings==== | ====b. Findings==== | ||
Line 372: | Line 353: | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors verified that there were no unplanned exposures or losses of radiological control over locked high radiation areas and very high radiation areas during the period from the third quarter 2013 through the third quarter 2014. The inspectors reviewed a sample of radiologically controlled area exit transactions showing exposures greater than | The inspectors verified that there were no unplanned exposures or losses of radiological control over locked high radiation areas and very high radiation areas during the period from the third quarter 2013 through the third quarter 2014. The inspectors reviewed a sample of radiologically controlled area exit transactions showing exposures greater than 100 mrem. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, to determine the accuracy of the reported data. | ||
These activities constituted verification of the occupational exposure control effectiveness performance indicator as defined in Inspection Procedure 71151. | These activities constituted verification of the occupational exposure control effectiveness performance indicator as defined in Inspection Procedure 71151. | ||
Line 379: | Line 360: | ||
No findings were identified. | No findings were identified. | ||
===.3 Radiological Effluent Technical Specifications (RETS)/Offsite Dose Calculation Manual (ODCM) Radiological Effluent Occurrences (PR01) | ===.3 Radiological Effluent Technical Specifications (RETS)/Offsite Dose Calculation Manual=== | ||
(ODCM) Radiological Effluent Occurrences (PR01) | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors reviewed corrective action program records for liquid or gaseous effluent releases that occurred from the third quarter 2013 through the third quarter 2014 and were reported to the NRC to verify the performance indicator data. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, | The inspectors reviewed corrective action program records for liquid or gaseous effluent releases that occurred from the third quarter 2013 through the third quarter 2014 and were reported to the NRC to verify the performance indicator data. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, to determine the accuracy of the reported data. | ||
These activities constituted verification of the radiological effluent technical specifications (RETS)/offsite dose calculation manual (ODCM) radiological effluent occurrences performance indicator as defined in Inspection Procedure | These activities constituted verification of the radiological effluent technical specifications (RETS)/offsite dose calculation manual (ODCM) radiological effluent occurrences performance indicator as defined in Inspection Procedure 71151. | ||
====b. Findings==== | ====b. Findings==== | ||
No findings were identified. | No findings were identified. {{a|4OA2}} | ||
==4OA2 Problem Identification and Resolution== | |||
{{IP sample|IP=IP 71152}} | |||
===.1 Routine Review=== | ===.1 Routine Review=== | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
Throughout the inspection period, the inspectors performed daily reviews of items entered into the | Throughout the inspection period, the inspectors performed daily reviews of items entered into the licensees corrective action program and periodically attended the licensees condition report screening meetings. The inspectors verified that licensee personnel were identifying problems at an appropriate threshold and entering these problems into the corrective action program for resolution. The inspectors verified that the licensee developed and implemented corrective actions commensurate with the significance of the problems identified. The inspectors also reviewed the licensees problem identification and resolution activities during the performance of the other inspection activities documented in this report. | ||
. The inspectors verified that licensee personnel were identifying problems at an appropriate threshold and entering these problems into the corrective action program for resolution. The inspectors verified that the licensee developed and implemented corrective actions commensurate with the significance of the problems identified. | |||
The inspectors also reviewed the | |||
====b. Findings==== | ====b. Findings==== | ||
No findings were identified. | No findings were identified. | ||
===.2 | ===.2 Semiannual Trend Review=== | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors reviewed the | The inspectors reviewed the licensees corrective action program, performance indicators, system health reports, and other documentation to identify trends that might indicate the existence of a more significant safety issue. The inspectors verified that the licensee was taking corrective actions to address identified adverse trends. | ||
These activities constitute completion of one semiannual trend review sample , | These activities constitute completion of one semiannual trend review sample, as defined in Inspection Procedure 71152. This sample reviewed the following condition reports (CR) and learning opportunities (LO): | ||
CR-CNS-2014-05233 | * CR-CNS-2014-05233 | ||
-assessment on operability reviews from July 29 through July 31, 2014. The station has received NRC | * CR-CNS-2014-05366 | ||
-identified findings associated with the failure to recognize the need for an evaluation and to properly document the bases for operability when a degraded nonconforming condition was identified and failure to follow the requirements of Station Procedure 0.5OPS, | * CR-CNS-2014-02290 | ||
* CR-CNS-2014-09663 | |||
* LO-2014-0051-20 b. Observations and Assessments The station performed a focused self-assessment on operability reviews from July 29 through July 31, 2014. The station has received NRC-identified findings associated with the failure to recognize the need for an evaluation and to properly document the bases for operability when a degraded nonconforming condition was identified and failure to follow the requirements of Station Procedure 0.5OPS, Operations Review of Condition Reports/Operability Determination. This assessment was performed to measure the effectiveness of changes to Station Procedure 0.5OPS. The period assessed was 1 year prior to the performance of the assessment. Additionally, the stations operability process was compared to industry best practices. | |||
The station identified the following observation during the assessment period: | The station identified the following observation during the assessment period: | ||
The station identified two examples where Station Procedure 0.5OPS is not completely aligned with NRC Inspection Manual Chapter 0326, | * The station identified two examples where Station Procedure 0.5OPS is not completely aligned with NRC Inspection Manual Chapter 0326, Operability Determinations and Functionality Assessments for Conditions Adverse to Quality and Safety, dated January 31, 2014, nor industry standards. | ||
Station Procedure 0.5OPS allowed up to 24 hours to complete an immediate determination prior to entering the prompt determination process. | |||
The definitions of prompt determination and operability evaluation are combined. Industry best practices contain a separate definition for operability evaluation thus removing any confusion that the senior reactor operator makes the determination. | |||
The station initiated Condition Report CR | The station initiated Condition Report CR-CNS-2014-05233 to capture this issue in the stations corrective action program. The station identified the following cause contributors: | ||
-CNS-2014-05233 to capture this issue in the | |||
1. Station Procedure 0.5OPS, Attachment 1, flowchart contains a decision block that if additional information is expected within 24 hours then to request engineering input to support an immediate determination. If the additional information is not expected with 24 hours, then the flowchart directs performance of an operability evaluation to support a prompt determination. | 1. Station Procedure 0.5OPS, Attachment 1, flowchart contains a decision block that if additional information is expected within 24 hours then to request engineering input to support an immediate determination. If the additional information is not expected with 24 hours, then the flowchart directs performance of an operability evaluation to support a prompt determination. | ||
2. The definitions of prompt determination and operability evaluation are combined definitions in Station Procedure 0.5OPS. The discussion regarding timeliness of prompt determinations from Inspection Manual Chapter 0326 and industry best practices was not included in the station | 2. The definitions of prompt determination and operability evaluation are combined definitions in Station Procedure 0.5OPS. The discussion regarding timeliness of prompt determinations from Inspection Manual Chapter 0326 and industry best practices was not included in the stations definition. | ||
The station implemented corrective actions to revise Station Procedure 0.5OPS to remove the allowance of 24 hours to perform an immediate determination. Also, the station separated the definitions of prompt determination and operability evaluation and included a discussion regarding timeliness of prompt determinations. | |||
The | The inspectors reviewed the focus self-assessment and Condition Report CR-CNS-2014-05233. The inspectors noted the following observation. Station Procedure 0.5OPS, Revision 52, contained the following definition for mission time, For operability determination purposes, the duration of structures, systems, and components operation that is credited in the design basis for the structures, systems, and components to perform its specified safety function (RIS 2005-20, Revision 1). | ||
, the | |||
Emergency diesel generators mission time is not specified in the current licensing basis and has been determined to be as long as the emergency diesel generators are required. | |||
The inspectors reviewed the current licensing basis and noted the following contained in USAR Section VII-5.2 Safety Design, | The inspectors reviewed the current licensing basis and noted the following contained in USAR Section VII-5.2 Safety Design, The diesel generator set shall be capable of automatic start at any time and capable of continued operation at rated load, voltage, and frequency until manually stopped. USAR Section XIV requires each diesel generator set to be operable for a 30 day mission time to support its safety objective for postulated design basis accidents. The station initiated Intranet Documents Control System 66781 to revise/clarify Station Procedure 0.5OPS to reflect the current licensing basis mission time for the emergency diesel generators. Additionally, the inspectors reviewed operability evaluations associated with the emergency diesel generators for the past year and did not identify any evaluations that used the inappropriate emergency diesel generator mission time. | ||
====c. Findings==== | ====c. Findings==== | ||
No findings were identified. | No findings were identified. | ||
===.3 Annual Follow=== | ===.3 Annual Follow-up of Selected Issues=== | ||
-up | ====a. Inspection Scope==== | ||
The inspectors selected three issues for an in-depth follow-up: | |||
* On October 28, 2014, CR-CNS-2014-01855, residual heat removal service water booster pump used as is non-conforming outlet piping. | |||
The inspectors assessed the licensees problem identification threshold, cause analyses, extent of condition reviews and compensatory actions. The inspectors verified that the licensee appropriately prioritized the planned corrective actions and that these actions were adequate to correct the condition. Specifically, verified corrective actions for use as is non-conforming schedule 30 piping on the residual heat removal service water booster pump outlet piping. | |||
* On November 5, 2014, CR-CNS-2014-02991, structural concrete strength 50.59 evaluation used to determine concrete strength based on 28 days test data. | |||
. Specifically, verified corrective actions for use as is non | |||
-conforming schedule 30 piping on the residual heat removal service water booster pump outlet piping. | |||
The inspectors assessed the licensees problem identification threshold, cause analyses, extent of condition reviews and compensatory actions. The inspectors verified that the licensee appropriately prioritized the planned corrective actions and that these actions were adequate to correct the condition. Specifically, verifying correction actions for verifying the correct concrete strength was identified for the inappropriate use of 5000 psi concrete for safety related structures. | |||
* On November 19, 2014, CR-CNS-2014-01505, diesel generator 1 and 2 used as is without valve stem keeper seals installed. | |||
. Specifically, verifying correction actions for verifying the correct concrete strength was identified for the inappropriate use of 5000 psi concrete for safety related structures. | |||
The inspectors assessed the licensees problem identification threshold, cause analyses, extent of condition reviews and compensatory actions. The inspectors verified that the licensee appropriately prioritized the planned corrective actions and that these actions were adequate to correct the condition. Specifically, corrective actions for not installing valve stem keeper seals on diesel generator 1 and 2. | |||
These activities constitute completion of three annual follow-up samples as defined | These activities constitute completion of three annual follow-up samples as defined in Inspection Procedure 71152. | ||
====b. Findings==== | ====b. Findings==== | ||
No findings were identified. | No findings were identified. {{a|4OA3}} | ||
==4OA3 Follow-up of Events and Notices of Enforcement Discretion== | |||
{{IP sample|IP=IP 71153}} | |||
These activities constitute completion of two event follow | These activities constitute completion of two event follow-up samples, as defined in Inspection Procedure 71153. | ||
-up samples, as defined in Inspection Procedure 71153. | |||
===.1 Dropped Control Rod=== | ===.1 Dropped Control Rod=== | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
On October | On October 11, 2014, the inspectors were informed by the control room that while removing Control Rod Blade 30-47 from the core, the control rod blade disengaged from the removal tool and dropped onto the reactor top guide. The inspectors monitored the licensees actions for control rod blade recovery, reviewed station logs, and reviewed NUREG-1022, Event Reporting Guidelines, Revision 3, to ensure licensee compliance. | ||
====b. Findings==== | ====b. Findings==== | ||
=====Introduction.===== | =====Introduction.===== | ||
The inspectors reviewed a self-revealing, Green, non | The inspectors reviewed a self-revealing, Green, non-cited violation of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, associated with the licensees failure to follow Special Procedure GEH-TP-116, Procedure for the Operation and Maintenance of the REM*TAKE-2/D-100 Modified REM*TAKE 2, Revision 3, for post-maintenance testing following corrective maintenance. | ||
-cited violation of 10 CFR Part 50, Appendix B, Criterion V, | |||
-2/D-100 Modified REM*TAKE 2, | |||
-maintenance testing following corrective maintenance. | |||
=====Description.===== | =====Description.===== | ||
On October 11, 2014, the licensee conducted control rod blade shuffles in support of Refueling Outage 28 operations. While removing Control | On October 11, 2014, the licensee conducted control rod blade shuffles in support of Refueling Outage 28 operations. While removing Control Rod Blade 30-47 from the core, the control rod blade disengaged from the REM*TAKE-2/D-100 removal tool and dropped onto the reactor core top guide. Follow-up reactor coolant water samples revealed that no reactor fuel was damaged during this event. The licensee subsequently initiated Condition Report CR-CNS-2014-06809. | ||
-2/D-100 removal tool and dropped onto the reactor core top guide. Follow-up reactor coolant water samples revealed that no reactor fuel was damaged during this event. The licensee subsequently initiated Condition Report CR | |||
-CNS-2014-06809. | |||
The inspectors determined that the failure to accomplish Step 7.2.4.7 resulted in the bleeder valve being out of calibration | The licensees root cause evaluation, performed under CR-CNS-2014-06809, determined that the dropping of Control Rod Blade 30-47 was caused by, the calibration of the bleeder valve [that] was not validated in accordance with Special Procedure GEH-TP-116, Procedure for the Operation and Maintenance of the REM*TAKE-2/D-100 Modified REM*TAKE 2, Revision 3, following corrective maintenance prior to operation of the REM*TAKE-2/D-100 tool. Specifically, Special Procedure GEH-TP-116, Step 7.2.4.7 was not completed, which defines the acceptable calibration of the bleeder valve. Specifcally, Step 7.2.4.7 states, that, Acceptable movement: The grippers should retract first and then 3 to 5 seconds later the control rod blade hook should actuate. This should be in sequence. If not, adjust the bleeder valve (turning clockwise to decrease flow or counter clockwise to increase flow) as needed and repeat Sections 7.2.4.4 through 7.2.4.6 until there is acceptable movement. The inspectors determined that the failure to accomplish Step 7.2.4.7 resulted in the bleeder valve being out of calibration, which nullified the fail-safe feature of the tool. With the fail-safe feature nullified, Control Rod Blade 30-47 became disengaged from the tool and dropped onto the reactor core when the supplemental employee inadvertently pressed the disengage button. | ||
, which nullified the fail | |||
-safe feature of the tool. | |||
The licensee subsequently identified that the station did not exercise sufficient oversight of the fuel handler contractor to verify that the fail-safe feature was fully functional after water clearing activities because the contractor was considered an expert in this type of work and in the use of the new type REM*TAKE-2/D-100 tool. The inspectors reviewed the licensees root cause analysis and determined that the identified root cause was reasonable. | |||
The licensee subsequently identified that the station did not exercise sufficient oversight of the fuel handler contractor to verify that the fail | |||
-safe feature was fully functional after water clearing activities because the contractor was considered an expert in this type of work and in the use of the new type REM*TAKE | |||
-2/D-100 tool. The inspectors reviewed the | |||
=====Analysis.===== | =====Analysis.===== | ||
The | The licensees failure to follow the post-maintenance testing requirements in Special Procedure GEH-TP-116 was a performance deficiency. The performance deficiency was more than minor, and therefore a finding, because it was associated with the human performance attribute of the Barrier Integrity Cornerstone and affected the associated objective of maintaining functionality of fuel cladding. Specifically, with the fail-safe nullified Control Rod Blade 30-47 became disengaged from the REM*TAKE-2/D-100 tool and dropped onto the reactor core top guide. Using Inspection Manual Chapter 0609, Appendix G, Attachment 1, Shutdown Operations Significance Determination Process Phase 1 Initial Screening and Characterization of Findings, dated May 09, 2014, inspectors determined that the finding was of very low safety significance (Green) because the finding did not impact the fuel barrier because it: | ||
: | : (1) does not increase the potential for failure of the freeze seal or if unmitigated have the potential to cause a disruption of residual heat removal/decay heat removal or a loss of inventory event; | ||
: (1) does not increase the potential for failure of the freeze seal or if unmitigated have the potential to cause a disruption of residual heat removal/decay heat removal or a loss of inventory event; (2)does not involve two or more adjacent control rods with the potential to, or actually, add postive reactivity; and (3)does not degrade the ability to isolate a drain down or leakage path. | : (2) does not involve two or more adjacent control rods with the potential to, or actually, add postive reactivity; and | ||
: (3) does not degrade the ability to isolate a drain down or leakage path. The finding has a cross-cutting aspect in the area of human performance associated with the field presence component because the licensee failed to ensure supervisory and management oversight of work activities, including contractors and supplemental personnel [H.2]. | |||
The finding has a cross | |||
-cutting aspect in the area of human performance associated with the field presence component because the licensee failed to ensure supervisory and management oversight of work activities, including contractors and supplemental personnel | |||
=====Enforcement.===== | =====Enforcement.===== | ||
Title 10 CFR Part 50, Appendix B, Criterion V, | Title 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, requires, in part, that activities affecting quality shall be prescribed by documented instructions, procedures, or drawings of a type appropriate to the circumstances and shall be accomplished in accordance with these instructions, procedures, and drawings. Safety-related Special Procedure GEH TP 116, Procedure for the Operation and Maintenance of the REM*TAKE 2/D 100 Modified REM*TAKE 2, Revision 3, Step 7.2.4.7, specified that, Acceptable movement: The grippers should retract first and then 3 to 5 seconds later the control rod blade hook should actuate. This should be in sequence. If not, adjust the bleeder valve (turning clockwise to decrease flow or counter clockwise to increase flow) as needed and repeat Sections 7.2.4.4 through 7.2.4.6 until there is acceptable movement. Contrary to the above, on October 10, 2014, the licensee failed to accomplish activities affecting quality in accordance with documented instructions appropriate to the circumstances. Specifically, the licensee failed to accomplish Step 7.2.4.7 of Special Procedure GEH-TP-116 which resulted in the bleeder valve being misadjusted and nullified the fail-safe feature of the REM*TAKE-2/D-100 tool. The licensees immediate corrective actions for the event was to suspended all in-vessel maintenance activities and remove REM*Take-2/D-100 grapple from service and determined functionality of the tool. Because this violation was of very low safety significance and was entered into the licensees corrective action program as Condition Report CR-CNS-2014-06809, this violation is being treated as a non-cited violation, consistent with Section 2.3.2.a of the NRCs Enforcement Policy. | ||
(NCV 05000298/2014005-01, Failure to Follow Procedure for Post Maintenance Testing) | |||
===.2 (Closed) Licensee Event Report (LER) 05000298/2014004-00, Implementation of=== | |||
Enforcement Guidance Memorandum 11-003, Revision 2, Causes Conditions Prohibited by Technical Specifications | |||
- | |||
===. | ====a. Inspection Scope==== | ||
During Refueling Outage 28, Cooper Nuclear Station performed Operations with a Potential for Draining the Reactor Vessel (OPDRV) activities while in Mode 5 without an operable secondary containment. An OPDRV is an activity that could result in the draining or siphoning of the reactor pressure vessel water level below the top of fuel, without crediting the use of mitigating measure to terminate the uncovering of fuel. | |||
Secondary containment is required by TS 3.6.4.1 to be operable during OPDRV. The required action for this specification is to suspend OPDRV operations. Therefore, entering the OPDRV without establishing secondary containment integrity was considered a condition prohibited by TS as defined by 10 CFR 50.73(a)(2)(i)(B). | |||
The NRC issued Enforcement Guidance Memorandum (EGM) 11-003, Revision 2, on December 13, 2013, to provide guidance on how to disposition boiling water reactor licensee noncompliances with TS containment requirements during OPDRV operations. | |||
The NRC considers enforcement discretion related to secondary containment operability during Mode 5 OPDRV activities appropriate because the associated interim actions necessary to receive the discretion ensure an adequate level of safety by requiring licensees immediate actions to: | |||
: (1) adhere to the NRC plain language meaning of OPDRV activities, | : (1) adhere to the NRC plain language meaning of OPDRV activities, | ||
: (2) meet the requirements which specify the minimum makeup flow rate and water inventory based on OPDRV activities with long drain down times, | : (2) meet the requirements which specify the minimum makeup flow rate and water inventory based on OPDRV activities with long drain down times, | ||
Line 530: | Line 487: | ||
: (4) ensure that licensees follow all other Mode 5 TS requirements for OPDRV activities. | : (4) ensure that licensees follow all other Mode 5 TS requirements for OPDRV activities. | ||
The inspectors reviewed this Licensee Event Report for potential performance deficiencies and/or violations of regulatory requirements. The inspectors reviewed the | The inspectors reviewed this Licensee Event Report for potential performance deficiencies and/or violations of regulatory requirements. The inspectors reviewed the stations implementation of the Enforcement Guidance Memorandum 11-003, Revision 2, during operations with a potential for draining the reactor vessel. Specific observations included: | ||
The inspectors observed that the operations with a potential for draining the reactor vessel activities were logged in the control room narrative logs, and that the log entry appropriately recorded the standby source of makeup designated for the evolutions. | |||
The inspectors noted that the reactor vessel water level was maintained at least greater than 21 feet above the top of the reactor pressure vessel flange as required by Technical Specification 3.9.6. The inspectors also verified that at least one safety-related pump was the standby source of makeup designed in the control room narrative logs for the evolutions. The inspectors confirmed that the worst case estimated time to drain the reactor cavity to the reactor pressure vessel flange was greater than 24 hours. | |||
-related pump was the standby source of makeup designed in the control room narrative logs for the evolutions. The inspectors confirmed that the worst case estimated time to drain the reactor cavity to the reactor pressure vessel flange was greater than 24 hours. | |||
The inspectors verified that the operations with a potential for draining the reactor vessels were not conducted in Mode 4 and that the licensee did not move irradiated fuel during the operations with a potential for draining the reactor vessels. The inspectors verified that two independent means of measuring reactor pressure vessel water level were available for identifying the onset of loss of inventory events. | |||
Technical Specification 3.6.4.1 requires, in part, that secondary containment shall be operable during operations with a potential for draining the reactor vessel. Technical Specification 3.6.4.1, Condition C, requires the licensee to initiate actions to suspend operations with a potential for draining the reactor vessel immediately when secondary containment is inoperable. Contrary to the above, from October 3, 2014 to October 22, 2014, Cooper Nuclear Station performed operations with a potential for draining the reactor vessel activities while in Mode 5 without an operable secondary containment. Specifically, the station conducted the following seven operations with a potential for draining the reactor vessel activities without an operable secondary containment: | Technical Specification 3.6.4.1 requires, in part, that secondary containment shall be operable during operations with a potential for draining the reactor vessel. Technical Specification 3.6.4.1, Condition C, requires the licensee to initiate actions to suspend operations with a potential for draining the reactor vessel immediately when secondary containment is inoperable. Contrary to the above, from October 3, 2014 to October 22, 2014, Cooper Nuclear Station performed operations with a potential for draining the reactor vessel activities while in Mode 5 without an operable secondary containment. Specifically, the station conducted the following seven operations with a potential for draining the reactor vessel activities without an operable secondary containment: | ||
Draining reactor recirculation pump without the jet pump plugs fully installed Control rod drive maintenance Removal of jet pump plugs associated with reactor recirculation pump B maintenance Venting the control rod drives Defeating the scram function for two control rod drives and support IVVI inspections Reactor recirculation pump A seal maintenance Control rod drive freeze seal These conditions were reported as conditions prohibited by Technical Specifications | * Draining reactor recirculation pump without the jet pump plugs fully installed | ||
* Control rod drive maintenance | |||
* Removal of jet pump plugs associated with reactor recirculation pump B maintenance | |||
* Venting the control rod drives | |||
* Defeating the scram function for two control rod drives and support IVVI inspections | |||
* Reactor recirculation pump A seal maintenance | |||
* Control rod drive freeze seal These conditions were reported as conditions prohibited by Technical Specifications. | |||
The licensee entered this issue into its corrective action program as Condition Reports CR-CNS-2014-06293. | |||
In accordance with EGM 11 | Since this violation occurred during the discretion period described in EGM 11-003, Revision 2, the NRC is exercising enforcement discretion in accordance with Section 3.5, Violations Involving Special Circumstances, of the NRC Enforcement Policy, and, therefore, will not issue enforcement action for this violation. | ||
-003, Revision 2, each licensee that receives discretion must submit a license amendment request within 4 months of the NRC | |||
In accordance with EGM 11-003, Revision 2, each licensee that receives discretion must submit a license amendment request within 4 months of the NRC staffs publication in the Federal Register of the notice of availability for a generic change to the standard TS to provide more clarity to the term OPDRV. | |||
The Licensee Event Report is closed. | The Licensee Event Report is closed. | ||
Line 549: | Line 514: | ||
====b. Findings==== | ====b. Findings==== | ||
No findings were identified. | No findings were identified. | ||
{{a|4OA5}} | |||
==4OA5 Other Activities== | |||
(Discussed) Temporary Instruction 2515/190 - Inspection of the Licensees Proposed Interim Actions as a Result of the Near-Term Task Force Recommendation 2.1 Flooding Reevaluation | |||
-Term Task Force Recommendation 2.1 Flooding Reevaluation | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspector(s) completed a partial verification that the | The inspector(s) completed a partial verification that the licensees interim actions would perform their intended function for some beyond design basis flooding events. However, the licensee has determined that additional flooding mitigation strategies and equipment will be necessary to address the full spectrum of potential beyond design basis flooding events at the Cooper Nuclear Station. This additional review is scheduled to be completed during the Spring of 2015 after the licensee submits their Flood Hazard Reevaluation Report (FHRR). As a result, an additional inspection activity using Temporary Instruction 2515/190 will be performed following the completion of the licensees review to verify that the additional strategies and equipment will perform their intended function for flooding mitigation. | ||
During the partial verification of the | During the partial verification of the licensees interim actions, the inspectors reviewed: | ||
* Flood monitoring procedures, including water level action trigger points (Phase 1) | |||
* Proposed beyond design basis flooding decay heat removal plan | |||
====b. Findings==== | ====b. Findings==== | ||
No findings were identified. | No findings were identified. | ||
{{a|4OA6}} | |||
==4OA6 Meetings, Including Exit== | |||
===Exit Meeting Summary=== | |||
On October 10, 2014, the inspectors presented the radiation safety inspection results to Mr. R. Penfield, Director, Nuclear Safety Assurance, and other members of the licensee staff. | |||
The licensee acknowledged the issues presented. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed. | |||
On October 10, 2014, the inspector presented the inspection results of the review of inservice inspection activities to Mr. K. Higginbotham, General Manager | On October 10, 2014, the inspector presented the inspection results of the review of inservice inspection activities to Mr. K. Higginbotham, General Manager, Plant Operations, and other members of the licensee staff. The licensee acknowledged the issues presented. | ||
, Plant Operations, and other members of the licensee staff. The licensee acknowledged the issues presented. | |||
The licensee confirmed that any proprietary information reviewed by the inspector had been returned or destroyed. | The licensee confirmed that any proprietary information reviewed by the inspector had been returned or destroyed. | ||
On December 8, 2014, the inspector presented the results of the in-office inspection of changes to the | On December 8, 2014, the inspector presented the results of the in-office inspection of changes to the licensees emergency plan to Ms. M. Ferguson, Manager, Emergency Preparedness, and other members of the licensee staff. The licensee acknowledged the issues presented. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed. | ||
On January 15, 2015, the inspectors presented the inspection results to Mr. O. Limpias , Vice President | On January 15, 2015, the inspectors presented the inspection results to Mr. O. Limpias, Vice President - Nuclear and Chief Nuclear Officer, and other members of the licensee staff. The licensee acknowledged the issues presented. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed. | ||
- Nuclear and Chief Nuclear Officer, and other members of the licensee staff. | |||
=SUPPLEMENTAL INFORMATION= | =SUPPLEMENTAL INFORMATION= | ||
Line 583: | Line 550: | ||
===Licensee Personnel=== | ===Licensee Personnel=== | ||
: [[contact::J. Bebb]], Staff Health Physicist | : [[contact::J. Bebb]], Staff Health Physicist | ||
: [[contact::J. Bednar]], Supervisor, Radiation Protection | : [[contact::J. Bednar]], Supervisor, Radiation Protection | ||
: [[contact::R. Beilke]], Manager, Radiation Protection | : [[contact::R. Beilke]], Manager, Radiation Protection | ||
: [[contact::S. | : [[contact::S. Carbonnet]], NDE Engineer | ||
: [[contact::P. Carlock]], Supervisor, Security Operations | : [[contact::P. Carlock]], Supervisor, Security Operations | ||
: [[contact::J. Dixon]], Supervisor, ALARA | : [[contact::J. Dixon]], Supervisor, ALARA | ||
: [[contact::S. Frieling]], Staff Health Physicist | : [[contact::S. Frieling]], Staff Health Physicist | ||
: [[contact::K. Higginbotham]], General Manager, Plant Operations | : [[contact::K. Higginbotham]], General Manager, Plant Operations | ||
: [[contact::J. | : [[contact::J. Hirner]], Respiratory Program Technician, Radiation Protection | ||
: [[contact::C. Hopple]], Radiological Protection Technician | : [[contact::C. Hopple]], Radiological Protection Technician | ||
: [[contact::B. Kirkpatrick]], | : [[contact::B. Kirkpatrick]], Licensing Specialist | ||
: [[contact::D. Madsen]], Licensing Engineer | |||
: [[contact::D. | : [[contact::T. McClure]], ISI Engineer | ||
: [[contact::T. | : [[contact::E. McCutchen]], Senior Licensing Engineer, Licensing | ||
: [[contact::E. | : [[contact::R. McDonald]], Senior Health Physicist, Radiation Protection | ||
: [[contact::R. | |||
: [[contact::J. Olberding]], Specialist, Licensing | : [[contact::J. Olberding]], Specialist, Licensing | ||
: [[contact::J. Shaw]], Manager, Licensing | : [[contact::J. Shaw]], Manager, Licensing | ||
: [[contact::J. | : [[contact::J. Smith]], Maintenance Weld Coordinator | ||
: [[contact::C. | : [[contact::C. Sunderman]], Assistant Training Manager, Radiation Protection | ||
: [[contact::K. Tanner]], Shift Supervisor, Radiation Protection | : [[contact::K. Tanner]], Shift Supervisor, Radiation Protection | ||
: [[contact::B. Thacker]], Supervisor, Codes Program | : [[contact::B. Thacker]], Supervisor, Codes Program | ||
Line 610: | Line 576: | ||
===Opened and Closed=== | ===Opened and Closed=== | ||
Failure to Follow Procedure for Post Maintenance Testing | |||
: 05000298/2014005-01 NCV (Section 4OA3) | |||
===Closed=== | ===Closed=== | ||
Implementation of Enforcement Guidance | |||
: 05000298/2014004-00 LER Memorandum 11-003, Revision 2, Causes Conditions Prohibited by Technical Specifications (Section 4OA3) | |||
=== | ===Discussed=== | ||
Inspection of the Licensees Proposed Interim Actions as a 2515/190 TI Result of the Near-Term Task Force Recommendation 2.1 Flooding Reevaluation (Section 4OA5) | |||
Attachment 1 | |||
==LIST OF DOCUMENTS REVIEWED== | |||
=== | |||
}} | }} |
Latest revision as of 05:55, 20 December 2019
ML15043A512 | |
Person / Time | |
---|---|
Site: | Cooper |
Issue date: | 02/11/2015 |
From: | Troy Pruett NRC/RGN-IV/DRP |
To: | Limpias O Nebraska Public Power District (NPPD) |
Groom J | |
References | |
EA-14-219 IR 2014005 | |
Download: ML15043A512 (48) | |
Text
UNITED STATES ary 11, 2015
SUBJECT:
COOPER NUCLEAR STATION - NRC INTEGRATED INSPECTION REPORT 05000298/2014005 AND EXERCISE OF ENFORCEMENT DISCRETION
Dear Mr. Limpias:
On December 31, 2014, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Cooper Nuclear Station. On January 15, 2015, the NRC inspectors discussed the results of this inspection with you and other members of your staff. Inspectors documented the results of this inspection in the enclosed inspection report.
NRC inspectors documented one finding of very low safety significance (Green) in this report.
This finding involved a violation of NRC requirements.
A violation involving the failure to maintain the operability of secondary containment during Operations with the Potential to Drain the Reactor Vessel (OPDRV) was identified. Specifically, from October 3, 2014, through October 22, 2014, Cooper Nuclear Station performed a total of 7 OPDRV activities with secondary containment inoperable in violation of Technical Specification 3.6.4.1, Secondary Containment. The NRC issued EGM 11-003, Enforcement Guidance Memorandum on Dispositioning Boiling Water Reactor Licensee Noncompliance with Technical Specification Containment Requirements During Operations with a Potential for Draining the Reactor Vessel, Revision 2, on December 13, 2013, allowing for the exercise of enforcement discretion for such OPDRV-related TS violations, when certain criteria are met.
The NRC concluded that Cooper Nuclear Station met these criteria. Therefore, I have been authorized, after consultation with the Director, Office of Enforcement to exercise enforcement discretion in accordance with Section 3.5, Violations Involving Special Circumstances, of the NRC Enforcement Policy and, therefore, will not issue enforcement action for this violation, subject to a timely license amendment request being submitted.
If you contest the violation or significance of the non-cited violation, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC resident inspector at the Cooper Nuclear Station. If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region IV; and the NRC resident inspector at the Cooper Nuclear Station.
In accordance with Title 10 of the Code of Federal Regulations (10 CFR) 2.390, Public Inspections, Exemptions, Requests for Withholding, a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRCs Public Document Room or from the Publicly Available Records (PARS) component of the NRC's Agencywide Documents Access and Management System (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Sincerely,
/RA T. Farnholtz for/
Troy Pruett Director Division of Reactor Projects Docket Nos. 50-298 License Nos. DPR-46
Enclosure:
Inspection Report 05000298/2014005 w/ Attachments:
1. Supplemental Information 2. Request for Information for the O
REGION IV==
Docket: 05000298 License: DPR-46 Report: 05000298/2014005 Licensee: Nebraska Public Power District Facility: Cooper Nuclear Station Location: 72676 648A Ave Brownville, NE Dates: October 1, 2014 through December 31, 2014 Inspectors: J. Josey, Senior Resident Inspector E. Coffman, Acting Senior Resident Inspector C. Henderson, Resident Inspector R. Azua, Senior Project Engineer M. Langelier, Project Engineer L. Carson II, Senior Health Physicist P. Hernandez, Health Physicist J. Drake, Senior Reactor Inspector P. Elkmann, Senior Emergency Preparedness Inspector Approved Jeremy Groom By: Acting Chief, Project Branch C Division of Reactor Projects-1- Enclosure
SUMMARY
IR 05000298/2014005; 10/01/2014 - 12/31/2014; Cooper Nuclear Station; Follow-up of Events and Notices of Enforcement Discretion.
The inspection activities described in this report were performed between October 1 and December 31, 2014, by the resident inspectors at the Cooper Nuclear Station and inspectors from the NRCs Region IV office. One finding of very low safety significance (Green) was documented in this report. This finding involved a violation of NRC requirements. The significance of inspection findings is indicated by their color (Green, White, Yellow, or Red),
which is determined using Inspection Manual Chapter 0609, Significance Determination Process. Their cross-cutting aspects are determined using Inspection Manual Chapter 0310,
Aspects within the Cross-Cutting Areas. Violations of NRC requirements are dispositioned in accordance with the NRC Enforcement Policy. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process.
Cornerstone: Barrier Integrity
- Green.
The inspectors reviewed a self-revealing, non-cited violation of 10 CFR Part 50,
Appendix B, Criterion V, Instructions, Procedures, and Drawings, associated with the licensees failure to follow Special Procedure GEH-TP-116, Procedure for the Operation and Maintenance of the REM*TAKE-2/D-100 Modified REM*TAKE 2, Revision 3, for post-maintenance testing following corrective maintenance. Specifically, the licensee did not follow post-maintenance testing requirements associated with the calibration of the bleeder valve for the REM*TAKE-2/D-100 tool following corrective maintenance to address water intrusion. This resulted in the bleeder valve being misadjusted and nullifying the fail-safe feature of the REM*TAKE-2/D-100 tool. With the fail-safe nullified, Control Rod Blade 30-47 became disengaged from the REM*TAKE-2/D-100 tool and dropped onto the reactor core top guide when the supplemental employee inadvertently pressed the disengage button. No reactor fuel was damaged as indicated by normal radiation levels and air samples on the refuel floor and reactor water coolant samples. The licensees immediate corrective actions for the event was to suspended all in-vessel maintenance activities and remove REM*Take-2/D-100 grapple from service and determined functionality of the tool. The licensee entered this deficiency into their corrective action program for resolution as Condition Report CR-CNS-2014-06809.
The licensees failure to follow the post-maintenance testing requirements in Special Procedure GEH-TP-116 was a performance deficiency. The performance deficiency was more than minor, and therefore a finding, because it was associated with the human performance attribute of the Barrier Integrity Cornerstone and affected the associated objective of maintaining functionality of fuel cladding. Specifically, with the fail-safe nullified,
Control Rod Blade 30-47 became disengaged from the REM*TAKE-2/D-100 tool and dropped onto the reactor core top guide when a supplemental employee inadvertently pressed the disengage button. Using Inspection Manual Chapter 0609, Appendix G,
Attachment 1, Shutdown Operations Significance Determination Process Phase 1 Initial Screening and Characterization of Findings, dated May 09, 2014, inspectors determined that the finding was of very low safety significance (Green) because the finding did not impact the fuel barrier because it: (1) does not increase the potential for failure of the freeze seal or if unmitigated have the potential to cause a disruption of residual heat removal/decay heat removal or a loss of inventory event; (2) does not involve two or more adjacent control rods with the potential to, or actually, add postive reactivity; and (3) does not degrade the ability to isolate a drain down or leakage path. The finding has a cross-cutting aspect in the area of human performance associated with the field presence component because the licensee failed to ensure supervisory and management oversight of work activities including contractors and supplemental personnel [H.2]. (Section 4OA3)
PLANT STATUS
The Cooper Nuclear Station began the inspection period shutdown for Refueling Outage 28, which began on September 27, 2014, during the previous quarter. On November 1, 2014, the station commenced reactor startup and the reactor was critical. On November 2, 2014, the station synchronized the main generator with the grid and began power ascension. The plant returned to full power on November 5, 2014, where it remained for the rest of the reporting period.
REPORT DETAILS
REACTOR SAFETY
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity
1R04 Equipment Alignment
Partial Walkdown
a. Inspection Scope
The inspectors performed partial system walk-downs of the following risk-significant systems:
- October 15, 2014, Residual heat removal shutdown cooling, Loop A
- November 5, 2014, Residual heat removal A low-pressure coolant injection during unplanned limiting condition for operation for residual heat removal B low-pressure coolant injection
- November 10, 2014, Standby gas treatment A The inspectors reviewed the licensees procedures and system design information to determine the correct lineup for the systems. They visually verified that critical portions of the systems were correctly aligned for the existing plant configuration.
These activities constituted three partial system walk-down samples as defined in Inspection Procedure 71111.04.
b. Findings
No findings were identified.
1R05 Fire Protection
.1 Quarterly Inspection
a. Inspection Scope
The inspectors evaluated the licensees fire protection program for operational status and material condition. The inspectors focused their inspection on four plant areas important to safety:
- October 4, 2014, Residual heat removal pump room, Fire Area I, Zone 1C
- October 8, 2014, Fire impairment for BLDG-DOOR-R209 and R208, Fire Area II, Zone 3A and Fire Area III, Zone 3B
- December 8, 2014, Battery room 1A, Fire Area IV(A), Zone 8E
- December 8, 2014, DC switchgear room 1A, Fire Area IV(A), Zone 8H For each area, the inspectors evaluated the fire plan against defined hazards and defense-in-depth features in the licensees fire protection program. The inspectors evaluated control of transient combustibles and ignition sources, fire detection and suppression systems, manual firefighting equipment and capability, passive fire protection features, and compensatory measures for degraded conditions.
These activities constituted four quarterly inspection samples, as defined in Inspection Procedure 71111.05.
b. Findings
No findings were identified.
.2 Annual Inspection
a. Inspection Scope
On November 21, 2014, the inspectors completed their annual evaluation of the licensees fire brigade performance. This evaluation included observation of an announced fire drill for the non-critical switchroom. During this drill, the inspectors evaluated the capability of the fire brigade members, the leadership ability of the brigade leader, the brigades use of turnout gear and fire-fighting equipment, and the effectiveness of the fire brigades team operation. The inspectors also reviewed whether the licensees fire brigade met NRC requirements for training, dedicated size and membership, and equipment.
These activities constituted one annual inspection sample, as defined in Inspection Procedure 71111.05.
b. Findings
No findings were identified.
1R07 Heat Sink Performance
a. Inspection Scope
On November 17, 2014, the inspectors completed an inspection of the readiness and availability of risk-significant heat exchangers. The inspectors observed performance testing, reviewed the data from the performance test, and verified the licensee used the industry standard periodic maintenance method outlined in EPRI NP-7552 for the B reactor equipment cooling heat exchanger. Additionally, the inspectors walked down the heat exchanger to observe its performance and material condition and verified that the heat exchanger was correctly categorized under the Maintenance Rule and was receiving the required maintenance.
These activities constitute completion of one heat sink performance annual review sample, as defined in Inspection Procedure 71111.07.
b. Findings
No findings were identified.
1R08 Inservice Inspection Activities
.1 Non-destructive Examination (NDE) Activities and Welding Activities
a. Inspection Scope
The inspectors directly observed the following nondestructive examinations:
SYSTEM WELD IDENTIFICATION EXAMINATION TYPE Main Steam MSH-152 Visual Reactor Vessel HME-88-3 Ultrasonic Reactor Vessel VC8-8C-6 Magnetic Particle The inspectors reviewed records for the following nondestructive examinations:
SYSTEM WELD IDENTIFICATION EXAMINATION TYPE Main Steam VR-DA-2 Visual Main Steam MS-S8 Visual Reactor Pressure PRE-BG1-1 Ultrasonic Vessel Reactor Pressure PRE-BG1-26 Ultrasonic Vessel Control Rod Drive CRD-26-51-1 Dye Penetrant Control Rod Drive CRD-26-03-1 Dye Penetrant Control Rod Drive CRD-30-03-1 Dye Penetrant During the review and observation of each examination, the inspectors observed whether activities were performed in accordance with the ASME Code requirements and applicable procedures. The inspectors also reviewed the qualifications of all nondestructive examination technicians performing the inspections to determine whether they were current.
The inspectors directly observed a portion of the following welding activities:
SYSTEM WELD IDENTIFICATION EXAMINATION TYPE Service Water FW-8 Shielded Metal Arc Welding Service Water FW-9 Shielded Metal Arc Welding Reactor Water RWCU-CV-15 FW-8 Gas Tungsten Arc Cleanup Welding The inspectors reviewed records for the following welding activities:
SYSTEM WELD IDENTIFICATION EXAMINATION TYPE Service Water FW-10 Shielded Metal Arc Welding Service Water FW-11 Shielded Metal Arc Welding The inspectors reviewed whether the welding procedure specifications and the welders had been properly qualified in accordance with ASME Code Section IX requirements.
The inspectors also determined whether essential variables were identified, recorded in the procedure qualification record, and formed the bases for qualification of the welding procedure specifications.
These activities constitute completion of one inservice inspection sample, as defined in Inspection Procedure 71111.08.
b. Findings
No findings were identified.
.2 Identification and Resolution of Problems
a. Inspection Scope
The inspectors reviewed 23 condition reports which dealt with inservice inspection activities and found the corrective actions for inservice inspection issues were appropriate. The specific condition reports reviewed are listed in the documents reviewed section. From this review, the inspectors concluded that the licensee has an appropriate threshold for entering inservice inspection issues into the corrective action program and has procedures that direct a root cause evaluation when necessary. The licensee also has an effective program for applying industry inservice inspection operating experience. Specific documents reviewed during this inspection are listed in the attachment.
These actions constitute completion of the requirements of Section 02.05.
b. Findings
No findings were identified.
1R11 Licensed Operator Requalification Program and Licensed Operator Performance
.1 Review of Licensed Operator Requalification
a. Inspection Scope
On November 19, 2014, the inspectors observed an evaluated simulator scenario performed by an operating crew. The inspectors assessed the performance of the operators and the evaluators critique of their performance. The inspectors also assessed the modeling and performance of the simulator during the requalification activities.
These activities constitute completion of one quarterly licensed operator requalification program sample, as defined in Inspection Procedure 71111.11.
b. Findings
No findings were identified.
.2 Review of Licensed Operator Performance
a. Inspection Scope
On November 1, 2014, the inspectors observed the performance of on-shift licensed operators in the plants main control room. At the time of the observations, the plant was in a period of heightened activity and risk due to reactor startup.
In addition, the inspectors assessed the operators adherence to plant procedures, including conduct of operations procedure, and other operations department policies.
These activities constitute completion of one quarterly licensed operator performance sample, as defined in Inspection Procedure 71111.11.
b. Findings
No findings were identified.
1R12 Maintenance Effectiveness
a. Inspection Scope
The inspectors reviewed two instances of degraded performance or condition of safety-related structures, systems, and components (SSCs):
- November 5, 2014, Reactor equipment cooling heat exchanger B
- December 16, 2014, 125 VDC charger 1A The inspectors reviewed the extent of condition of possible common cause structure, system, and component failures and evaluated the adequacy of the licensees corrective actions. The inspectors reviewed the licensees work practices to evaluate whether these may have played a role in the degradation of the structure, system, or component.
The inspectors assessed the licensees characterization of the degradation in accordance with 10 CFR 50.65 (the Maintenance Rule), and verified that the licensee was appropriately tracking degraded performance and conditions in accordance with the Maintenance Rule.
These activities constituted completion of two maintenance effectiveness samples, as defined in Inspection Procedure 71111.12.
b. Findings
No findings were identified.
1R13 Maintenance Risk Assessments and Emergent Work Control
a. Inspection Scope
The inspectors reviewed four risk assessments performed by the licensee prior to changes in plant configuration and the risk management actions taken by the licensee in response to elevated risk:
- October 20, 2014, 4160 VAC, Bus G outage
- November 1, 2014, Dredging in the area of the intake structure barrage impact
- November 4, 2014, Technical Specification Limiting Condition for Operation 3.0.4.b risk evaluation, Mode 1 and 2 entry with SW-AOV-TCV451B unavailable
- November 24, 2014, Temporary fans associated with alternate decay heat removal room The inspectors verified that these risk assessments were performed timely and in accordance with the requirements of 10 CFR 50.65 (the Maintenance Rule) and plant procedures. The inspectors reviewed the accuracy and completeness of the licensees risk assessments and verified that the licensee implemented appropriate risk management actions based on the result of the assessments.
The inspectors also observed portions of two emergent work activities that had the potential to affect the functional capability of mitigating systems.
- November 12, 2014, Residual heat removal injection valve RHR-MOV-27B failing to open
- November 12, 2014, Diesel generator 2, 3R cylinder injector pump replacement The inspectors verified that the licensee appropriately developed and followed a work plan for these activities. The inspectors verified that the licensee took precautions to minimize the impact of the work activities on unaffected structures, systems, and components (SSCs).
These activities constitute completion of six maintenance risk assessments and emergent work control inspection samples, as defined in Inspection Procedure 71111.13.
b. Findings
No findings were identified.
1R15 Operability Determinations and Functionality Assessments
a. Inspection Scope
The inspectors reviewed four operability determinations and functionality assessments that the licensee performed for degraded or nonconforming structures, systems, or components (SSCs):
- November 18, 2014, CR-CNS-2014-06602, Operability determination of 480 VAC, Bus G, anchor bolts
- November 18, 2014, CR-CNS-2014-07552 and CR-CNS-2014-07978, Operability determination of Division I service water system SW-V-108 failed to open during post-loss of coolant accident flow to control room air conditioner
- November 19, 2014, Operability determination of secondary containment with railroad inner airlock door open
- December 15, 2014, CR-CNS-2014-08280 and CR-CNS-2014-08316, Functionality assessment of reactor core isolation cooling steam leak on drip leg trap inlet The inspectors reviewed the timeliness and technical adequacy of the licensees evaluations. Where the licensee determined the degraded structure, system, or component to be operable or functional, the inspectors verified that the licensees compensatory measures were appropriate to provide reasonable assurance of operability or functionality. The inspectors verified that the licensee had considered the effect of other degraded conditions on the operability or functionality of the degraded structure, system, or component.
These activities constitute completion of four operability and functionality review samples, as defined in Inspection Procedure 71111.15.
b. Findings
No findings were identified.
1R18 Plant Modifications
a. Inspection Scope
The inspectors reviewed two permanent plant modifications that affected risk-significant structures, systems, and components (SSCs):
- October 7, 2014, modification to address 125 VDC battery rack B non-conforming bolting configuration
- October 27, 2014, HPCI-MO-14 valve replacement change evaluation document 6017820 The inspectors reviewed the design and implementation of the modifications. The inspectors verified that work activities involved in implementing the modifications did not adversely impact operator actions that may be required in response to an emergency or other unplanned event. The inspectors verified that post-modification testing was adequate to establish the operability of the structures, systems, and components as modified.
These activities constitute completion of two samples of permanent modifications, as defined in Inspection Procedure 71111.18.
b. Findings
No findings were identified.
1R19 Post-Maintenance Testing
a. Inspection Scope
The inspectors reviewed six post-maintenance testing activities that affected risk-significant structures, systems, or components (SSCs):
- October 21, 2014, Z sump pump Z1 high high level switch replacement
- October 22, 2014, Diesel generator 2 fuel oil injection pumps replacement
- October 27, 2014, Main steam isolation valve 80A, 80D, 86A, and 86D air operated and manifold maintenance
- November 4, 2014, 125/250 VDC B battery replacement
- November 4, 2014, Diesel generator 1 6-year inspection and maintenance
- November 4, 2014, HPCI-MOV-14 replacement The inspectors reviewed licensing and design-basis documents for the structures, systems, and components, and the maintenance and post-maintenance test procedures.
The inspectors observed the performance of the post-maintenance tests to verify that the licensee performed the tests in accordance with approved procedures, satisfied the established acceptance criteria, and restored the operability of the affected structures, systems, and components.
These activities constitute completion of six post-maintenance testing inspection samples, as defined in Inspection Procedure 71111.19.
b. Findings
No findings were identified.
1R20 Refueling and Other Outage Activities
a. Inspection Scope
During the stations refueling outage that concluded on November 2, 2014, the inspectors evaluated the licensees outage activities. The inspectors verified that the licensee considered risk in developing and implementing the outage plan, appropriately managed personnel fatigue, and developed mitigation strategies for losses of key safety functions. This verification included the following:
- Review of the licensees outage plan prior to the outage
- Monitoring of shut-down and cool-down activities
- Verification that the licensee maintained defense-in-depth during outage activities
- Observation and review of operations with a potential for draining the reactor vessel
- Observation and review of fuel handling activities
- Monitoring of heat-up and startup activities These activities constitute completion of one refueling outage sample, as defined in Inspection Procedure 71111.20.
b. Findings
No findings were identified.
1R22 Surveillance Testing
a. Inspection Scope
The inspectors observed five risk-significant surveillance tests and reviewed test results to verify that these tests adequately demonstrated that the structures, systems, and components (SSCs) were capable of performing their safety functions:
In-service tests:
- November 4, 2014, High pressure coolant injection Containment isolation valve surveillance tests:
- October 6, 2014, Primary containment isolation valves RR-AO-740 and RR-AO-741 operability and closure timing test Other surveillance tests:
- October 27, 2014, Reactor core isolation coolant local leak rate test RWCU-15CV, RCIC-MOV-15, and RCIC-MOV-16
- November 1, 2014, Main steam line isolation valve local leak rate testing
- November 3, 2014, Control rod drive hatch local leak-rate test The inspectors verified that these tests met technical specification requirements, that the licensee performed the tests in accordance with their procedures, and that the results of the test satisfied appropriate acceptance criteria. The inspectors verified that the licensee restored the operability of the affected structures, systems, and components following testing.
These activities constitute completion of five surveillance testing inspection samples, as defined in Inspection Procedure 71111.22.
b. Findings
No findings were identified.
Cornerstone: Emergency Preparedness
1EP4 Emergency Action Level and Emergency Plan Changes
a. Inspection Scope
The inspector performed an in-office review of the Cooper Nuclear Station Emergency Plan, Revision 65, dated June 23, 2014. This revision:
- Defined hostile action
- Added detail about the process for requesting offsite assistance for fire fighting
- Added detail about the telephone connectivity between the licensees site and its Emergency Operations Facility
- Added detail about the radio communications systems available to the Operations and Security departments during an emergency
- Added a requirement to maintain satellite phones in the licensees Control Room, Technical Support Center, Emergency Operations Facility, and Joint Information Center
- Added a requirement to maintain informational signs for the public using the Steamboat Trace Trail
- Deleted a requirement to maintain respiratory protection equipment (self-contained breathing apparatus) at the Communications Building
- Deleted references to the use of the Auburn Rescue Squad and Nemaha County Hospital Rescue Squad in transporting injured station personnel to medical facilities
- Corrected typographical errors and titles, and made other administrative changes This revision was compared to its previous revision, to the criteria of NUREG-0654, Criteria for Preparation and Evaluation of Radiological Emergency Response Plans and Preparedness in Support of Nuclear Power Plants, Revision 1, and to the standards in 10 CFR 50.47(b) to determine if the revision adequately implemented the requirements of 10 CFR 50.54(q)(3) and 50.54(q)(4). The inspector verified that the revision did not decrease the effectiveness of the emergency plan. This review was not documented in a safety evaluation report and did not constitute approval of licensee-generated changes; therefore, this revision is subject to future inspection.
These activities constitute completion of one emergency action level and emergency plan changes sample as defined in Inspection Procedure 71114.04.
b. Findings
No findings were identified.
RADIATION SAFETY
Cornerstones: Public Radiation Safety and Occupational Radiation Safety
2RS1 Radiological Hazard Assessment and Exposure Controls
a. Inspection Scope
The inspectors assessed the licensees performance in assessing the radiological hazards in the workplace associated with licensed activities. The inspectors assessed the licensees implementation of appropriate radiation monitoring and exposure control measures for both individual and collective exposures. The inspectors walked down various portions of the plant and performed independent radiation dose rate measurements. The inspectors interviewed the radiation protection manager, radiation protection supervisors, and radiation workers. The inspectors reviewed licensee performance in the following areas:
- The hazard assessment program, including a review of the licensees evaluations of changes in plant operations and radiological surveys to detect dose rates, airborne radioactivity, and surface contamination levels
- Instructions and notices to workers, including labeling or marking containers of radioactive material, radiation work permits, actions for electronic dosimeter alarms, and changes to radiological conditions
- Programs and processes for control of sealed sources and release of potentially contaminated material from the radiologically controlled area, including survey performance, instrument sensitivity, release criteria, procedural guidance, and sealed source accountability
- Radiological hazards control and work coverage, including the adequacy of surveys, radiation protection job coverage and contamination controls, the use of electronic dosimeters in high noise areas, dosimetry placement, airborne radioactivity monitoring, controls for highly activated or contaminated materials (non-fuel) stored within spent fuel and other storage pools, and posting and physical controls for high radiation areas and very high radiation areas
- Radiation worker and radiation protection technician performance with respect to radiation protection work requirements
- Audits, self-assessments, and corrective action documents related to radiological hazard assessment and exposure controls since the last inspection These activities constitute completion of one sample of radiological hazard assessment and exposure controls as defined in Inspection Procedure 71124.01.
b. Findings
No findings were identified.
2RS3 In-Plant Airborne Radioactivity Control and Mitigation
a. Inspection Scope
The inspectors evaluated whether the licensee controlled in-plant airborne radioactivity concentrations consistent with ALARA principles and that the use of respiratory protection devices did not pose an undue risk to the wearer. During the inspection, the inspectors interviewed licensee personnel, walked down various portions of the plant, and reviewed licensee performance in the following areas:
- The licensees use, when applicable, of ventilation systems as part of its engineering controls
- The licensees respiratory protection program for use, storage, maintenance, and quality assurance of National Institute for Occupational Safety and Health (NIOSH)-certified equipment, qualification and training of personnel, and user performance
- The licensees capability for refilling and transporting self-contained breathing apparatus (SCBA) air bottles to and from the control room and operations support center during emergency conditions, status of self-contained breathing apparatus staged and ready for use in the plant and associated surveillance records, and personnel qualification and training
- Audits, self-assessments, and corrective action documents related to in-plant airborne radioactivity control and mitigation since the last inspection These activities constitute completion of one sample of in-plant airborne radioactivity control and mitigation as defined in Inspection Procedure 71124.03.
b. Findings
No findings were identified.
OTHER ACTIVITIES
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Security
4OA1 Performance Indicator Verification
.1 Mitigating System Performance Index: Emergency AC Power Systems (MS06), High
Pressure Injection Systems (MS07), Heat Removal Systems (MS08), Residual Heat Removal Systems (MS09), and Cooling Water Systems (MS10)
a. Inspection Scope
The inspectors reviewed the licensees mitigating system performance index data for the period of September 22, 2013 through September 30, 2014, to verify the accuracy and completeness of the reported data. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, to determine the accuracy of the reported data.
These activities constituted verification of the mitigating system performance index for emergency ac power systems, high pressure injection systems, heat removal systems, residual heat removal systems, and cooling water systems, as defined in Inspection Procedure 71151.
b. Findings
No findings were identified.
.2 Occupational Exposure Control Effectiveness (OR01)
a. Inspection Scope
The inspectors verified that there were no unplanned exposures or losses of radiological control over locked high radiation areas and very high radiation areas during the period from the third quarter 2013 through the third quarter 2014. The inspectors reviewed a sample of radiologically controlled area exit transactions showing exposures greater than 100 mrem. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, to determine the accuracy of the reported data.
These activities constituted verification of the occupational exposure control effectiveness performance indicator as defined in Inspection Procedure 71151.
b. Findings
No findings were identified.
.3 Radiological Effluent Technical Specifications (RETS)/Offsite Dose Calculation Manual
(ODCM) Radiological Effluent Occurrences (PR01)
a. Inspection Scope
The inspectors reviewed corrective action program records for liquid or gaseous effluent releases that occurred from the third quarter 2013 through the third quarter 2014 and were reported to the NRC to verify the performance indicator data. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, to determine the accuracy of the reported data.
These activities constituted verification of the radiological effluent technical specifications (RETS)/offsite dose calculation manual (ODCM) radiological effluent occurrences performance indicator as defined in Inspection Procedure 71151.
b. Findings
No findings were identified.
4OA2 Problem Identification and Resolution
.1 Routine Review
a. Inspection Scope
Throughout the inspection period, the inspectors performed daily reviews of items entered into the licensees corrective action program and periodically attended the licensees condition report screening meetings. The inspectors verified that licensee personnel were identifying problems at an appropriate threshold and entering these problems into the corrective action program for resolution. The inspectors verified that the licensee developed and implemented corrective actions commensurate with the significance of the problems identified. The inspectors also reviewed the licensees problem identification and resolution activities during the performance of the other inspection activities documented in this report.
b. Findings
No findings were identified.
.2 Semiannual Trend Review
a. Inspection Scope
The inspectors reviewed the licensees corrective action program, performance indicators, system health reports, and other documentation to identify trends that might indicate the existence of a more significant safety issue. The inspectors verified that the licensee was taking corrective actions to address identified adverse trends.
These activities constitute completion of one semiannual trend review sample, as defined in Inspection Procedure 71152. This sample reviewed the following condition reports (CR) and learning opportunities (LO):
- LO-2014-0051-20 b. Observations and Assessments The station performed a focused self-assessment on operability reviews from July 29 through July 31, 2014. The station has received NRC-identified findings associated with the failure to recognize the need for an evaluation and to properly document the bases for operability when a degraded nonconforming condition was identified and failure to follow the requirements of Station Procedure 0.5OPS, Operations Review of Condition Reports/Operability Determination. This assessment was performed to measure the effectiveness of changes to Station Procedure 0.5OPS. The period assessed was 1 year prior to the performance of the assessment. Additionally, the stations operability process was compared to industry best practices.
The station identified the following observation during the assessment period:
- The station identified two examples where Station Procedure 0.5OPS is not completely aligned with NRC Inspection Manual Chapter 0326, Operability Determinations and Functionality Assessments for Conditions Adverse to Quality and Safety, dated January 31, 2014, nor industry standards.
Station Procedure 0.5OPS allowed up to 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> to complete an immediate determination prior to entering the prompt determination process.
The definitions of prompt determination and operability evaluation are combined. Industry best practices contain a separate definition for operability evaluation thus removing any confusion that the senior reactor operator makes the determination.
The station initiated Condition Report CR-CNS-2014-05233 to capture this issue in the stations corrective action program. The station identified the following cause contributors:
1. Station Procedure 0.5OPS, Attachment 1, flowchart contains a decision block that if additional information is expected within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> then to request engineering input to support an immediate determination. If the additional information is not expected with 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />, then the flowchart directs performance of an operability evaluation to support a prompt determination.
2. The definitions of prompt determination and operability evaluation are combined definitions in Station Procedure 0.5OPS. The discussion regarding timeliness of prompt determinations from Inspection Manual Chapter 0326 and industry best practices was not included in the stations definition.
The station implemented corrective actions to revise Station Procedure 0.5OPS to remove the allowance of 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> to perform an immediate determination. Also, the station separated the definitions of prompt determination and operability evaluation and included a discussion regarding timeliness of prompt determinations.
The inspectors reviewed the focus self-assessment and Condition Report CR-CNS-2014-05233. The inspectors noted the following observation. Station Procedure 0.5OPS, Revision 52, contained the following definition for mission time, For operability determination purposes, the duration of structures, systems, and components operation that is credited in the design basis for the structures, systems, and components to perform its specified safety function (RIS 2005-20, Revision 1).
Emergency diesel generators mission time is not specified in the current licensing basis and has been determined to be as long as the emergency diesel generators are required.
The inspectors reviewed the current licensing basis and noted the following contained in USAR Section VII-5.2 Safety Design, The diesel generator set shall be capable of automatic start at any time and capable of continued operation at rated load, voltage, and frequency until manually stopped. USAR Section XIV requires each diesel generator set to be operable for a 30 day mission time to support its safety objective for postulated design basis accidents. The station initiated Intranet Documents Control System 66781 to revise/clarify Station Procedure 0.5OPS to reflect the current licensing basis mission time for the emergency diesel generators. Additionally, the inspectors reviewed operability evaluations associated with the emergency diesel generators for the past year and did not identify any evaluations that used the inappropriate emergency diesel generator mission time.
c. Findings
No findings were identified.
.3 Annual Follow-up of Selected Issues
a. Inspection Scope
The inspectors selected three issues for an in-depth follow-up:
- On October 28, 2014, CR-CNS-2014-01855, residual heat removal service water booster pump used as is non-conforming outlet piping.
The inspectors assessed the licensees problem identification threshold, cause analyses, extent of condition reviews and compensatory actions. The inspectors verified that the licensee appropriately prioritized the planned corrective actions and that these actions were adequate to correct the condition. Specifically, verified corrective actions for use as is non-conforming schedule 30 piping on the residual heat removal service water booster pump outlet piping.
- On November 5, 2014, CR-CNS-2014-02991, structural concrete strength 50.59 evaluation used to determine concrete strength based on 28 days test data.
The inspectors assessed the licensees problem identification threshold, cause analyses, extent of condition reviews and compensatory actions. The inspectors verified that the licensee appropriately prioritized the planned corrective actions and that these actions were adequate to correct the condition. Specifically, verifying correction actions for verifying the correct concrete strength was identified for the inappropriate use of 5000 psi concrete for safety related structures.
- On November 19, 2014, CR-CNS-2014-01505, diesel generator 1 and 2 used as is without valve stem keeper seals installed.
The inspectors assessed the licensees problem identification threshold, cause analyses, extent of condition reviews and compensatory actions. The inspectors verified that the licensee appropriately prioritized the planned corrective actions and that these actions were adequate to correct the condition. Specifically, corrective actions for not installing valve stem keeper seals on diesel generator 1 and 2.
These activities constitute completion of three annual follow-up samples as defined in Inspection Procedure 71152.
b. Findings
No findings were identified.
4OA3 Follow-up of Events and Notices of Enforcement Discretion
These activities constitute completion of two event follow-up samples, as defined in Inspection Procedure 71153.
.1 Dropped Control Rod
a. Inspection Scope
On October 11, 2014, the inspectors were informed by the control room that while removing Control Rod Blade 30-47 from the core, the control rod blade disengaged from the removal tool and dropped onto the reactor top guide. The inspectors monitored the licensees actions for control rod blade recovery, reviewed station logs, and reviewed NUREG-1022, Event Reporting Guidelines, Revision 3, to ensure licensee compliance.
b. Findings
Introduction.
The inspectors reviewed a self-revealing, Green, non-cited violation of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, associated with the licensees failure to follow Special Procedure GEH-TP-116, Procedure for the Operation and Maintenance of the REM*TAKE-2/D-100 Modified REM*TAKE 2, Revision 3, for post-maintenance testing following corrective maintenance.
Description.
On October 11, 2014, the licensee conducted control rod blade shuffles in support of Refueling Outage 28 operations. While removing Control Rod Blade 30-47 from the core, the control rod blade disengaged from the REM*TAKE-2/D-100 removal tool and dropped onto the reactor core top guide. Follow-up reactor coolant water samples revealed that no reactor fuel was damaged during this event. The licensee subsequently initiated Condition Report CR-CNS-2014-06809.
The licensees root cause evaluation, performed under CR-CNS-2014-06809, determined that the dropping of Control Rod Blade 30-47 was caused by, the calibration of the bleeder valve [that] was not validated in accordance with Special Procedure GEH-TP-116, Procedure for the Operation and Maintenance of the REM*TAKE-2/D-100 Modified REM*TAKE 2, Revision 3, following corrective maintenance prior to operation of the REM*TAKE-2/D-100 tool. Specifically, Special Procedure GEH-TP-116, Step 7.2.4.7 was not completed, which defines the acceptable calibration of the bleeder valve. Specifcally, Step 7.2.4.7 states, that, Acceptable movement: The grippers should retract first and then 3 to 5 seconds later the control rod blade hook should actuate. This should be in sequence. If not, adjust the bleeder valve (turning clockwise to decrease flow or counter clockwise to increase flow) as needed and repeat Sections 7.2.4.4 through 7.2.4.6 until there is acceptable movement. The inspectors determined that the failure to accomplish Step 7.2.4.7 resulted in the bleeder valve being out of calibration, which nullified the fail-safe feature of the tool. With the fail-safe feature nullified, Control Rod Blade 30-47 became disengaged from the tool and dropped onto the reactor core when the supplemental employee inadvertently pressed the disengage button.
The licensee subsequently identified that the station did not exercise sufficient oversight of the fuel handler contractor to verify that the fail-safe feature was fully functional after water clearing activities because the contractor was considered an expert in this type of work and in the use of the new type REM*TAKE-2/D-100 tool. The inspectors reviewed the licensees root cause analysis and determined that the identified root cause was reasonable.
Analysis.
The licensees failure to follow the post-maintenance testing requirements in Special Procedure GEH-TP-116 was a performance deficiency. The performance deficiency was more than minor, and therefore a finding, because it was associated with the human performance attribute of the Barrier Integrity Cornerstone and affected the associated objective of maintaining functionality of fuel cladding. Specifically, with the fail-safe nullified Control Rod Blade 30-47 became disengaged from the REM*TAKE-2/D-100 tool and dropped onto the reactor core top guide. Using Inspection Manual Chapter 0609, Appendix G, Attachment 1, Shutdown Operations Significance Determination Process Phase 1 Initial Screening and Characterization of Findings, dated May 09, 2014, inspectors determined that the finding was of very low safety significance (Green) because the finding did not impact the fuel barrier because it:
- (1) does not increase the potential for failure of the freeze seal or if unmitigated have the potential to cause a disruption of residual heat removal/decay heat removal or a loss of inventory event;
- (2) does not involve two or more adjacent control rods with the potential to, or actually, add postive reactivity; and
- (3) does not degrade the ability to isolate a drain down or leakage path. The finding has a cross-cutting aspect in the area of human performance associated with the field presence component because the licensee failed to ensure supervisory and management oversight of work activities, including contractors and supplemental personnel [H.2].
Enforcement.
Title 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, requires, in part, that activities affecting quality shall be prescribed by documented instructions, procedures, or drawings of a type appropriate to the circumstances and shall be accomplished in accordance with these instructions, procedures, and drawings. Safety-related Special Procedure GEH TP 116, Procedure for the Operation and Maintenance of the REM*TAKE 2/D 100 Modified REM*TAKE 2, Revision 3, Step 7.2.4.7, specified that, Acceptable movement: The grippers should retract first and then 3 to 5 seconds later the control rod blade hook should actuate. This should be in sequence. If not, adjust the bleeder valve (turning clockwise to decrease flow or counter clockwise to increase flow) as needed and repeat Sections 7.2.4.4 through 7.2.4.6 until there is acceptable movement. Contrary to the above, on October 10, 2014, the licensee failed to accomplish activities affecting quality in accordance with documented instructions appropriate to the circumstances. Specifically, the licensee failed to accomplish Step 7.2.4.7 of Special Procedure GEH-TP-116 which resulted in the bleeder valve being misadjusted and nullified the fail-safe feature of the REM*TAKE-2/D-100 tool. The licensees immediate corrective actions for the event was to suspended all in-vessel maintenance activities and remove REM*Take-2/D-100 grapple from service and determined functionality of the tool. Because this violation was of very low safety significance and was entered into the licensees corrective action program as Condition Report CR-CNS-2014-06809, this violation is being treated as a non-cited violation, consistent with Section 2.3.2.a of the NRCs Enforcement Policy.
(NCV 05000298/2014005-01, Failure to Follow Procedure for Post Maintenance Testing)
.2 (Closed) Licensee Event Report (LER) 05000298/2014004-00, Implementation of
Enforcement Guidance Memorandum 11-003, Revision 2, Causes Conditions Prohibited by Technical Specifications
a. Inspection Scope
During Refueling Outage 28, Cooper Nuclear Station performed Operations with a Potential for Draining the Reactor Vessel (OPDRV) activities while in Mode 5 without an operable secondary containment. An OPDRV is an activity that could result in the draining or siphoning of the reactor pressure vessel water level below the top of fuel, without crediting the use of mitigating measure to terminate the uncovering of fuel.
Secondary containment is required by TS 3.6.4.1 to be operable during OPDRV. The required action for this specification is to suspend OPDRV operations. Therefore, entering the OPDRV without establishing secondary containment integrity was considered a condition prohibited by TS as defined by 10 CFR 50.73(a)(2)(i)(B).
The NRC issued Enforcement Guidance Memorandum (EGM) 11-003, Revision 2, on December 13, 2013, to provide guidance on how to disposition boiling water reactor licensee noncompliances with TS containment requirements during OPDRV operations.
The NRC considers enforcement discretion related to secondary containment operability during Mode 5 OPDRV activities appropriate because the associated interim actions necessary to receive the discretion ensure an adequate level of safety by requiring licensees immediate actions to:
- (1) adhere to the NRC plain language meaning of OPDRV activities,
- (2) meet the requirements which specify the minimum makeup flow rate and water inventory based on OPDRV activities with long drain down times,
- (3) ensure that adequate defense in depth is maintained to minimize the potential for the release of fission products with secondary containment not operable by
- (a) monitoring RPV level to identify the onset of a loss of inventory event,
- (b) maintaining the capability to isolate the potential leakage paths,
- (c) prohibiting Mode 4 (cold shutdown) OPDRV activities, and
- (d) prohibiting movement of irradiated fuel with the spent fuel storage pool gates removed in Mode 5, and
- (4) ensure that licensees follow all other Mode 5 TS requirements for OPDRV activities.
The inspectors reviewed this Licensee Event Report for potential performance deficiencies and/or violations of regulatory requirements. The inspectors reviewed the stations implementation of the Enforcement Guidance Memorandum 11-003, Revision 2, during operations with a potential for draining the reactor vessel. Specific observations included:
The inspectors observed that the operations with a potential for draining the reactor vessel activities were logged in the control room narrative logs, and that the log entry appropriately recorded the standby source of makeup designated for the evolutions.
The inspectors noted that the reactor vessel water level was maintained at least greater than 21 feet above the top of the reactor pressure vessel flange as required by Technical Specification 3.9.6. The inspectors also verified that at least one safety-related pump was the standby source of makeup designed in the control room narrative logs for the evolutions. The inspectors confirmed that the worst case estimated time to drain the reactor cavity to the reactor pressure vessel flange was greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.
The inspectors verified that the operations with a potential for draining the reactor vessels were not conducted in Mode 4 and that the licensee did not move irradiated fuel during the operations with a potential for draining the reactor vessels. The inspectors verified that two independent means of measuring reactor pressure vessel water level were available for identifying the onset of loss of inventory events.
Technical Specification 3.6.4.1 requires, in part, that secondary containment shall be operable during operations with a potential for draining the reactor vessel. Technical Specification 3.6.4.1, Condition C, requires the licensee to initiate actions to suspend operations with a potential for draining the reactor vessel immediately when secondary containment is inoperable. Contrary to the above, from October 3, 2014 to October 22, 2014, Cooper Nuclear Station performed operations with a potential for draining the reactor vessel activities while in Mode 5 without an operable secondary containment. Specifically, the station conducted the following seven operations with a potential for draining the reactor vessel activities without an operable secondary containment:
- Draining reactor recirculation pump without the jet pump plugs fully installed
- Control rod drive maintenance
- Removal of jet pump plugs associated with reactor recirculation pump B maintenance
- Venting the control rod drives
- Defeating the scram function for two control rod drives and support IVVI inspections
- Reactor recirculation pump A seal maintenance
- Control rod drive freeze seal These conditions were reported as conditions prohibited by Technical Specifications.
The licensee entered this issue into its corrective action program as Condition Reports CR-CNS-2014-06293.
Since this violation occurred during the discretion period described in EGM 11-003, Revision 2, the NRC is exercising enforcement discretion in accordance with Section 3.5, Violations Involving Special Circumstances, of the NRC Enforcement Policy, and, therefore, will not issue enforcement action for this violation.
In accordance with EGM 11-003, Revision 2, each licensee that receives discretion must submit a license amendment request within 4 months of the NRC staffs publication in the Federal Register of the notice of availability for a generic change to the standard TS to provide more clarity to the term OPDRV.
The Licensee Event Report is closed.
b. Findings
No findings were identified.
4OA5 Other Activities
(Discussed) Temporary Instruction 2515/190 - Inspection of the Licensees Proposed Interim Actions as a Result of the Near-Term Task Force Recommendation 2.1 Flooding Reevaluation
a. Inspection Scope
The inspector(s) completed a partial verification that the licensees interim actions would perform their intended function for some beyond design basis flooding events. However, the licensee has determined that additional flooding mitigation strategies and equipment will be necessary to address the full spectrum of potential beyond design basis flooding events at the Cooper Nuclear Station. This additional review is scheduled to be completed during the Spring of 2015 after the licensee submits their Flood Hazard Reevaluation Report (FHRR). As a result, an additional inspection activity using Temporary Instruction 2515/190 will be performed following the completion of the licensees review to verify that the additional strategies and equipment will perform their intended function for flooding mitigation.
During the partial verification of the licensees interim actions, the inspectors reviewed:
- Flood monitoring procedures, including water level action trigger points (Phase 1)
- Proposed beyond design basis flooding decay heat removal plan
b. Findings
No findings were identified.
4OA6 Meetings, Including Exit
Exit Meeting Summary
On October 10, 2014, the inspectors presented the radiation safety inspection results to Mr. R. Penfield, Director, Nuclear Safety Assurance, and other members of the licensee staff.
The licensee acknowledged the issues presented. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed.
On October 10, 2014, the inspector presented the inspection results of the review of inservice inspection activities to Mr. K. Higginbotham, General Manager, Plant Operations, and other members of the licensee staff. The licensee acknowledged the issues presented.
The licensee confirmed that any proprietary information reviewed by the inspector had been returned or destroyed.
On December 8, 2014, the inspector presented the results of the in-office inspection of changes to the licensees emergency plan to Ms. M. Ferguson, Manager, Emergency Preparedness, and other members of the licensee staff. The licensee acknowledged the issues presented. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed.
On January 15, 2015, the inspectors presented the inspection results to Mr. O. Limpias, Vice President - Nuclear and Chief Nuclear Officer, and other members of the licensee staff. The licensee acknowledged the issues presented. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed.
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
Licensee Personnel
- J. Bebb, Staff Health Physicist
- J. Bednar, Supervisor, Radiation Protection
- R. Beilke, Manager, Radiation Protection
- S. Carbonnet, NDE Engineer
- P. Carlock, Supervisor, Security Operations
- S. Frieling, Staff Health Physicist
- K. Higginbotham, General Manager, Plant Operations
- J. Hirner, Respiratory Program Technician, Radiation Protection
- C. Hopple, Radiological Protection Technician
- B. Kirkpatrick, Licensing Specialist
- D. Madsen, Licensing Engineer
- T. McClure, ISI Engineer
- E. McCutchen, Senior Licensing Engineer, Licensing
- R. McDonald, Senior Health Physicist, Radiation Protection
- J. Olberding, Specialist, Licensing
- J. Shaw, Manager, Licensing
- C. Sunderman, Assistant Training Manager, Radiation Protection
- K. Tanner, Shift Supervisor, Radiation Protection
- B. Thacker, Supervisor, Codes Program
- T. Whistler, Radiological Protection Technician
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
Opened and Closed
Failure to Follow Procedure for Post Maintenance Testing
- 05000298/2014005-01 NCV (Section 4OA3)
Closed
Implementation of Enforcement Guidance
- 05000298/2014004-00 LER Memorandum 11-003, Revision 2, Causes Conditions Prohibited by Technical Specifications (Section 4OA3)
Discussed
Inspection of the Licensees Proposed Interim Actions as a 2515/190 TI Result of the Near-Term Task Force Recommendation 2.1 Flooding Reevaluation (Section 4OA5)
Attachment 1