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Category:Letter
MONTHYEARML24250A2052024-10-0808 October 2024 Issuance of Amendment No. 278 Regarding Revision to Technical Specification Table 3.3.2.1-1 and Transfer of Minimum Critical Power Ratio Values to Core Operating Limit Report ML24227A0822024-09-0303 September 2024 Summary of Regulatory Audit in Support of License Amendment Request to Modify the High Pressure Coolant Injection Low Flow Value IR 05000298/20240052024-08-22022 August 2024 Updated Inspection Plan for Cooper Nuclear Station (Report 05000298/2024005) IR 05000298/20240022024-07-25025 July 2024 Integrated Inspection Report 05000298/2024002 ML24183A1722024-07-17017 July 2024 Issuance of Amendment No. 277 to Adopt TSTF-374, Revision to TS 5.5.13 and Associated TS Bases for Diesel Fuel Oil ML24197A1462024-07-15015 July 2024 NRC Region IV Ltr to Cooper Nuclear Station Re FEMA Level 1 Finding IR 05000298/20243012024-07-12012 July 2024 NRC Examination Report 05000298/2024301 ML24134A1782024-07-0303 July 2024 Issuance of Amendment No. 276 Revision to Technical Specification 3.8.3, Diesel Fuel Oil, Lube Oil and Starting Air, to Allow for Cleaning, Inspection and Any Needed Repairs During Refuel Outage 33 ML24197A0682024-06-24024 June 2024 FEMA Ltr to Missouri State Emergency Management Agency - Level 1 Finding, 24 June 2024 ML24192A0112024-06-13013 June 2024 2024-06-Post Exam Comments 05000298/LER-2023-002-01, Secondary Containment Differential Pressure Perturbation Exceeds Technical Specifications2024-06-0606 June 2024 Secondary Containment Differential Pressure Perturbation Exceeds Technical Specifications IR 05000298/20244012024-06-0404 June 2024 Security Baseline Inspection Report 05000298/2024401 ML24151A1082024-05-30030 May 2024 NRC Initial Operator Licensing Examination Approval 05000298/2024301 ML24137A0942024-05-17017 May 2024 Regulatory Audit Plan in Support of License Amendment Request to Modify Allowable Value Regarding Technical Specification for High Pressure Coolant Injection Pump Discharge Low Flow 05000298/LER-2024-005, High Pressure Coolant Injection Pressure Switch Installation Causes Condition That Could Have Prevented Fulfillment of a Safety Function and a Condition Prohibited B Technical2024-05-13013 May 2024 High Pressure Coolant Injection Pressure Switch Installation Causes Condition That Could Have Prevented Fulfillment of a Safety Function and a Condition Prohibited B Technical. 05000298/LER-2024-004, Main Turbine Stop Valve Position Switches Do Not Meet Channel Independence Criteria Results in Two Channels Being Declared Inoperable and a Condition Prohibited by Technical Specifications2024-05-0909 May 2024 Main Turbine Stop Valve Position Switches Do Not Meet Channel Independence Criteria Results in Two Channels Being Declared Inoperable and a Condition Prohibited by Technical Specifications IR 05000298/20240012024-05-0303 May 2024 Integrated Inspection Report 05000298/2024001 ML24129A0952024-04-25025 April 2024 Preparation and Scheduling of Operator Licensing Examinations IR 05000298/20240102024-04-24024 April 2024 Comprehensive Engineering Team Inspection Report 05000298/2024010 ML24096A1202024-04-0505 April 2024 Issuance of Amendment No. 275 Revision to Technical Specification 3.3.1.1 (Emergency Circumstances) ML24093A2282024-04-0202 April 2024 Notice of Enforcement Discretion for Cooper Nuclear Station IR 05000298/20240902024-04-0101 April 2024 – Notice of Violation, NRC Inspection Report 05000298/2024090 IR 05000298/20230062024-02-28028 February 2024 Annual Assessment Letter for Cooper Nuclear Station - Report 05000298/2023006 ML24033A3092024-02-12012 February 2024 Summary of Regulatory Audit Regarding the Relief Request RC3-02 Regarding Drywell Head Bolting IR 05000298/20230042024-02-12012 February 2024 Integrated Inspection Report 05000298/2023004 IR 05000298/20230122024-02-12012 February 2024 NRC Inspection Report 05000298/2023012 ML23334A2012024-01-0303 January 2024 Issuance of Amendment No. 274 Revision to Technical Specifications to Adopt TSTF-551, Revision 3, Revise Secondary Containment Surveillance Requirements ML23311A2082023-11-0909 November 2023 Reassignment of U.S. Nuclear Regulatory Commission Branch Chief in the Division of Operating Reactor Licensing for Plant Licensing Branch IV ML23311A1122023-11-0909 November 2023 Project Manager Assignment IR 05000298/20230032023-11-0202 November 2023 Integrated Inspection Report 05000298/2023003 IR 05000298/20234012023-11-0101 November 2023 Cyber Security Report 05000298/2023401 Public ML23264A8052023-10-11011 October 2023 Issuance of Amendment No. 273 Revision to Technical Specifications to Adopt TSTF-580, Revision 1, Provide Exception from Entering Mode 4 with No Operable RHR Shutdown Cooling ML23233A1882023-09-0505 September 2023 Regulatory Audit Plan in Support of Relief Request RC3-02 Regarding Drywell Head Bolting IR 05000298/20230052023-08-21021 August 2023 Updated Inspection Plan for Cooper Nuclear Station (Report 05000298/2023005)- Mid Cycle Letter IR 05000298/20230022023-08-0808 August 2023 Integrated Inspection Report 05000298/2023002 ML23214A2742023-08-0303 August 2023 Nuclear Station - Notification of Inspection (NRC Inspection Report 05000298/2023004) and Request for Information IR 05000298/20234022023-08-0303 August 2023 NRC Security Inspection Report 05000298/2023402 IR 05000298/20234202023-08-0101 August 2023 Security Baseline Inspection Report 05000298/2023420 ML23173A0862023-06-26026 June 2023 Information Request for the Cybersecurity Baseline Inspection, Notification to Perform Inspection 05000298/2023401 IR 05000298/20230102023-05-17017 May 2023 Biennial Problem Identification and Resolution Inspection Report 05000298/2023010 IR 05000298/20234032023-05-0404 May 2023 Security Baseline Inspection Report 05000298/2023403 ML23129A2822023-04-20020 April 2023 Submittal of Revision 31 to Updated Safety Analysis Report ML23102A0282023-04-19019 April 2023 U.S. Nuclear Regulatory Commission Presentation at the May 8, 2023, Brownville Village Meeting IR 05000298/20230012023-04-17017 April 2023 Integrated Inspection Report 05000298/2023001 ML23060A1582023-03-0808 March 2023 Design Basis Assurance Inspection (Programs) Inspection Report 05000298/2023001 IR 05000298/20220062023-03-0101 March 2023 Annual Assessment Letter for Cooper Nuclear Station Report 05000298/2022006 ML23041A1622023-02-10010 February 2023 Licensed Operator Positive Fitness-for-Duty Test Request for Additional Information IR 05000298/20220042023-01-30030 January 2023 Integrated Inspection Report 05000298/2022004 IR 05000298/20220112022-12-23023 December 2022 License Renewal Phase 4 Inspection Report 05000298/2022011 ML22286A2072022-11-30030 November 2022 Issuance of Amendment No. 272 Revision to Technical Specifications to Adopt TSTF-554, Revision 1, Revise Reactor Coolant Leakage Requirements 2024-09-03
[Table view] Category:Licensee Event Report (LER)
MONTHYEAR05000298/LER-2023-002-01, Secondary Containment Differential Pressure Perturbation Exceeds Technical Specifications2024-06-0606 June 2024 Secondary Containment Differential Pressure Perturbation Exceeds Technical Specifications 05000298/LER-2024-005, High Pressure Coolant Injection Pressure Switch Installation Causes Condition That Could Have Prevented Fulfillment of a Safety Function and a Condition Prohibited B Technical2024-05-13013 May 2024 High Pressure Coolant Injection Pressure Switch Installation Causes Condition That Could Have Prevented Fulfillment of a Safety Function and a Condition Prohibited B Technical. 05000298/LER-2024-004, Main Turbine Stop Valve Position Switches Do Not Meet Channel Independence Criteria Results in Two Channels Being Declared Inoperable and a Condition Prohibited by Technical Specifications2024-05-0909 May 2024 Main Turbine Stop Valve Position Switches Do Not Meet Channel Independence Criteria Results in Two Channels Being Declared Inoperable and a Condition Prohibited by Technical Specifications NLS2024035, Main Turbine Stop Valve Position Switches Do Not Meet Channel Independence Criteria Results in Two Channels Being Declared Inoperable and a Condition Prohibited by Technical Specifications2024-05-0909 May 2024 Main Turbine Stop Valve Position Switches Do Not Meet Channel Independence Criteria Results in Two Channels Being Declared Inoperable and a Condition Prohibited by Technical Specifications NLS2024029, High Pressure Coolant Injection Steam Leak Causes Condition That Could Have Prevented Fulfillment of a Safety Function and a Condition Prohibited by Technical Specifications2024-04-22022 April 2024 High Pressure Coolant Injection Steam Leak Causes Condition That Could Have Prevented Fulfillment of a Safety Function and a Condition Prohibited by Technical Specifications NLS2024013, Inoperable Turbine Stop Valve Limit Switch Causes Condition Prohibited by Technical Specifications2024-03-0404 March 2024 Inoperable Turbine Stop Valve Limit Switch Causes Condition Prohibited by Technical Specifications NLS2024014, Technical Specifications Prohibited Condition for Inoperable Service Water Booster Pump2024-03-0404 March 2024 Technical Specifications Prohibited Condition for Inoperable Service Water Booster Pump 05000298/LER-2016-0012017-09-27027 September 2017 De-Energized High Pressure Coolant Injection Auxiliary Lube Oil Pump Caused by Relay Failure Results in Loss of Safety Function and a Condition Prohibited by Technical Specifications, LER 16-001-01 for Cooper Nuclear Station Regarding De-Energized High Pressure Coolant Injection Auxiliary Lube Oil Pump Caused by Relay Failure Results in Loss of Safety Function, a Condition Prohibited by Tech Specs, and a 10 CFR Part 21 Report 05000298/LER-2017-0052017-08-17017 August 2017 Traversing In-core Probe In-shield Limit Switch Mounting Failure Results in Common Cause Inoperability of Independent Trains or Channels and Condition Prohibited by Technical Specifications, LER 17-005-00 for Cooper Nuclear Station Regarding Traversing In-core Probe In-shield Limit Switch Mounting Failure Results in Common Cause lnoperability of Independent Trains or Channels and Condition Prohibited by Technical Specifications 05000298/LER-2017-0042017-08-17017 August 2017 Torus to Drywell Vacuum Breaker Failure to Indicate Full Closed Causes Loss of Safety Function, LER 17-004-00 for Cooper Nuclear Station Regarding Torus to Drywall Vacuum Breaker Failure to Indicate Full Closed Causes Loss of Safety Function 05000298/LER-2017-0032017-07-24024 July 2017 Mispositioned Control Room Emergency Filter System Supply Fan Damper Causes Loss of Safety Function, LER 17-003-00 for Cooper Nuclear Station re Mispositioned Control Room Emergency Filter System Supply Fan Damper Causes Loss of Safety Function 05000298/LER-2017-0022017-04-27027 April 2017 Valve Test Failures Result in Condition Prohibited by Technical Specifications and a Loss of Safety Function, LER 17-002-00 for Cooper Nuclear Station Regarding Valve Test Failures Result in Condition Prohibited by Technical Specifications and a Loss of Safety Function 05000298/LER-2017-0012017-04-0505 April 2017 Residual Heat Removal Minimum Flow Valves OUt of Position Results in Loss of Safety Function and Condition Prohibited by Technical Specifications, LER 17-001-00 for Cooper Regarding Residual Heat Removal Minimum Flow Valves Out of Position Results in Loss of Safety Function and Condition Prohibited by Technical Specifications 05000298/LER-2016-0082017-01-0505 January 2017 Purchase and Installation of Incorrect Actuator Results in a Condition Prohibited by Technical Specifications, LER 16-008-00 for Cooper Nuclear Station Regarding Purchase and Installation of Incorrect Actuator Results in a Condition Prohibited by Technical Specifications 05000298/LER-2016-0062016-12-19019 December 2016 High Vibration on Control Room Emergency Filter System Fan Results in Inoperability and Loss of Safety Function, LER-16-006-00 for Cooper Nuclear Station Regarding High Vibration on Control Room Emergency Filter System Fan Results in Inoperability and Loss of Safety Function 05000298/LER-2016-0072016-12-19019 December 2016 Isolation of Shutdown Cooling due to Relay Maintenance Results in a Loss of Safety Function, LER 16-007-00 for Cooper Nuclear Station Regarding Isolation of Shutdown Cooling due to Relay Maintenance Results in a Loss of Safety Function 05000298/LER-2016-0042016-11-22022 November 2016 Closure of Multiple Main Steam Isolation Valves due to High Flow Signal, LER 16-004-00 for Cooper Nuclear Station Regarding Closure of Multiple Main Steam Isolation Valves due to High Flow Signal 05000298/LER-2016-0032016-11-0909 November 2016 Scaffold Construction Places Plant in a Condition Prohibited by Technical Specifications, LER 16-003-00 for Cooper Nuclear Station RE: Scaffold Construction Places Plant in a Condition Prohibited by Technical Specifications 05000298/LER-2016-0022016-06-27027 June 2016 De-Energized High Pressure Coolant Injection Auxiliary Lube Oil Pump Caused By Light Bulb Failure Results in Loss of Safety Function, LER 16-002-00 for Cooper Regarding De-Energized High Pressure Coolant Injection Auxiliary Lube Oil Pump Caused By Light Bulb Failure Results in Loss of Safety Function NLS2015063, Retraction of Licensee Event Report 2014-005-00, Lube Oil Leak Results in a Potential Condition Prohibited by Technical Specifications and a Potential Loss of Safety Function.2015-06-0909 June 2015 Retraction of Licensee Event Report 2014-005-00, Lube Oil Leak Results in a Potential Condition Prohibited by Technical Specifications and a Potential Loss of Safety Function. ML13149A1722013-05-26026 May 2013 E-mail from Micheal Mulligan to R.Guzman, Pilgrim Evacuation Plan Broken During Blizzard Nemo and Unenforced by the Nrc. NLS2013015, Special Report, Offgas Treatment System Charcoal Adsorbers Out of Service2013-01-29029 January 2013 Special Report, Offgas Treatment System Charcoal Adsorbers Out of Service NLS2008058, LER 08-S01-00 for Cooper Regarding Temporary Suspension of Security Measures Due to Tornado Warning2008-08-0505 August 2008 LER 08-S01-00 for Cooper Regarding Temporary Suspension of Security Measures Due to Tornado Warning 2024-06-06
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LER-2023-002, Secondary Containment Differential Pressure Perturbation Exceeds Technical Specifications |
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N Nebraska Public Power District "Always there when you need us"
10 CFR 50.73
NLS2024044 June 6, 2024
ATTN: Document Control Desk U.S. Nuclear Regulatory Commission Washington, D.C. 20555-0001
Subject: Licensee Event Report No. 2023-002-01 Cooper Nuclear Station, Docket No. 50-298, DPR-46
Dear Sir or Madam:
The purpose of this correspondence is to forward Licensee Event Report 2023-002-01.
This letter does not contain regulatory commitments.
Sincerely, I
halil Dia Site Vice President
/jo
Attachment: Licensee Event Report 2023-002-01
cc: Regional Administrator w/attachment NPG Distribution w/attachment USNRC - Region IV
Cooper Project Manager w/attachment INPO Records Center w/attachment USNRC - NRR Plant Licensing Branch IV via IRIS entry
Senior Resident Inspector w/attachment SORC Chairman w/attachment USNRC-CNS
SRAB Administrator w/attachment CNS Records w/attachment
COOPER NUCLEAR STATION 72676 648A Ave/ P.O. Box 98 I Brownville, NE 68321 http://www.nppd.com
Abstract
On October 22, 2023, Reactor Building pressure exceeded the Technical Specifications limit of -0.25 inches of water gauge (wg) resulting in Secondary Containment being declared inoperable.
Operations personnel walked down the ventilation systems and found that the first discharge duct hatch for EF-R-1 B was open. The hatch was subsequently closed, and Secondary Containment pressure returned to the normal operating set point of -0.33 inches wg.
The cause of the event was the opened first discharge duct hatch for EF-R-1 B. The cause of the open hatch has been determined to be looseness of the latching mechanism likely due to normal vibrations from system operations.
There was no impact on nuclear safety, plant reliability, radiological safety, or industrial safety.
Event Notification 56811 was submitted on October 22, 2023, due to the unplanned inoperability of Secondary Containment.
PLANT STATUS
Cooper Nuclear Station was in Mode 1, Power Operation, at 100 percent power at the time of the event on October 22, 2023.
Both Standby Gas Treatment (SGT) [EIIS: BH] trains were in normal standby lineup. Reactor Building Heating and Ventilation (RB HV) [EIIS: VA] was controlling Secondary Containment pressure. Single exhaust fan EF-R-1 B was in service, with an indicated exhaust flow rate of 35,000 standard cubic feet per minute, for cold weather operation.
BACKGROUND
Secondary Containment serves as a barrier to confine and monitor potential releases during fuel handling operations and is a system that limits the release of radioactive materials to the environment and consists of four subsystems. One of the subsystems is the Reactor Building [EIIS: NG], which encloses the Reactor Pressure Vessel [EIIS: RPV] and Primary Containment [EIIS: NH].
The Secondary Containment area (most of the Reactor Building) has supply and exhaust ventilating systems.
The supply system furnishes filtered 100% outdoor air to all floors of the building through ductwork. The supply unit has an operating and standby (100% capacity) fan, each with vortex dampers [EIIS: COMP], which deliver supply air at a rate proportional to a static pneumatic signal set manually by operations personnel.
The exhaust air is induced from the ventilated areas to a common plenum connected to the two exhaust fans, each of 100% capacity. The air is then exhausted to the atmosphere.
During normal plant operation, a minimum average negative pressure (vacuum) of 0.25 inches of water gauge (wg) is maintained by differential pressure (DP) controllers which receive signals proportional to the pressure difference between outside air and the Secondary Containment atmosphere, and control the position of the exhaust fan vortex dampers. The DP is detected by four separate probes, with one on each side of the Reactor Building. Control action is initiated from the average value of the four sensor probes.
If a Loss of Coolant Accident should occur, all ventilation systems of the Primary Containment area and Secondary Containment area will trip, Secondary Containment is isolated automatically, and the SGT system will be automatically initiated.
Each exhaust fan has a transition piece between the round fan barrel and the following rectangular duct work.
Each exhaust fan has an air operated discharge damper installed in the duct work immediately downstream of the transition piece. On each exhaust fan discharge duct, there is a duct hatch on the upstream side of the NRC FORM 366A (04-02-2024) U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY 0MB: NO. 3150-0104 EXPIRES: 04/30/2027 Cooper Nuclear Station 05000-298 NUMBER NO.
2023 002 01
discharge damper, and a duct hatch on the downstream side of the discharge damper. These hatches are on the side of the duct, hinged for horizontal swing, with two securing latches. There are also access hatches on top of each of the exhaust ducts in the overhead of the refuel floor. These exhaust ducts must contain positive pressure relative to building ambient air and relative to atmosphere. If a hatch fails to stay closed, some of the exhaust air flows out of the duct and re-circulates. This causes reduced mass air flow to atmosphere, an initial increase in Secondary Containment pressure, and reduced vacuum (reduced DP to atmosphere).
EVENT DESCRIPTION
On October 22, 2023, at 1149 hours0.0133 days <br />0.319 hours <br />0.0019 weeks <br />4.371945e-4 months <br />, control room operators noted that Reactor Building pressure had exceeded the Technical Specification (TS) Limiting Condition for Operation (LCO) of -0.25 inches wg.
Maximum Secondary Containment pressure was -0.13 inches wg. Reactor Building Heating and Ventilation (RB HV) was configured for cold weather operation and low air flow rate, with a single exhaust fan, EF-R-1 B, in service. Due to the pressure transient being above -0.25 inches wg, control room operators declared Secondary Containment inoperable at 1150 hours0.0133 days <br />0.319 hours <br />0.0019 weeks <br />4.37575e-4 months <br />, and entered TS LCO 3.6.4.1, Condition A, Required Action A.1, to restore Secondary Containment to operable status. The Reactor Building Ventilation System responded without operator action to restore DP to within TS limits at 1151 hours0.0133 days <br />0.32 hours <br />0.0019 weeks <br />4.379555e-4 months <br />.
Plant conditions and meteorological data were reviewed to determine the cause of the DP transient. The results of this review determined that the transient was not attributable to meteorological conditions. Operators also determined that the transient was not attributable to equipment operations, maintenance, or plant manipulation, such as RB HV supply unit air filter changes, or initiating or securing auxiliary steam to the RB HV supply unit.
Operations personnel continued to investigate by walking down the ventilation systems. At 1310 hours0.0152 days <br />0.364 hours <br />0.00217 weeks <br />4.98455e-4 months <br />, operations personnel found that the first discharge duct hatch for EF-R-1 B was open. The hatch was subsequently closed and Secondary Containment pressure returned to the normal operating set point of -0.33 inches wg. Operations personnel declared Secondary Containment OPERABLE and exited LCO 3.6.4.1, Condition A.
BASIS FOR REPORT
This event is reportable under 10 CFR 50. 73(a)(2)(v)(C and D) - An event or condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to control the release of radioactive material or mitigate the consequences of an accident. Event Notification 56811 was submitted on October 22, 2023, due to the unplanned inoperability of Secondary Containment. NRC FORM 366A (04-02-2024) U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY 0MB: NO. 3150-0104 EXPIRES: 04/30/2027 Cooper Nuclear Station 05000-298 NUMBER NO.
2023 002 01
SAFETY SIGNIFICANCE
This event is non-consequential. The pressure excursion in the Reactor Building resulted in an unexpected plant condition and met the entry condition for required action pursuant to Technical Specifications. This event resulted in failure to meet Secondary Containment TS LCO 3.6.4.1 for approximately 80 seconds. Secondary Containment pressure remained sub-atmospheric throughout the event. The non-essential reactor building HVAC system automatically restored required pressure (simple restoration).
An engineering review demonstrated that the perturbation on Secondary Containment pressure caused by the non-essential HVAC system did not impact the integrity of Secondary Containment or the ability of SGT to maintain Secondary Containment at a negative pressure. The first discharge duct hatch for EF-R-1 B is located inside the Secondary Containment isolation boundary and would be isolated in an accident.
As such, this event will not be counted as a Safety System Functional Failure for the Nuclear Regulatory Commission performance indicator since no loss of safety function occurred.
CAUSE
The cause of the event was the opened first discharge duct hatch for EF-R-1 B. The cause of the open hatch has been determined to be looseness of the latching mechanism likely due to normal vibrations from system operations.
CORRECTIVE ACTIONS
Operations personnel closed and verified the duct hatch was secured.
Cooper Nuclear Station will examine RB HV ventilation ductwork hatches and repair as needed.
PREVIOUS EVENTS
On May 23, 2022 - Secondary Containment was declared inoperable due to a rise in differential pressure. This was reported under LER 2022-001-00 as a loss of safety function under 10 CFR 50. 73(a)(2)(v)(C and D) - An event or condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to control the release of radioactive material or mitigate the consequences of an accident.
On February 9, 2021 - Secondary Containment was declared inoperable due to a rise in differential pressure.
This was reported under LER 2021-001-00 as a loss of safety function under 10 CFR 50.73(a)(2)(v)(C and D) -
An event or condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to control the release of radioactive material or mitigate the consequences of an accident. NRC FORM 366A (04-02-2024) U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY 0MB: NO. 3150-0104 EXPIRES: 04/30/2027 Cooper Nuclear Station 05000-298 NUMBER NO.
2023 002 01
On November 3, 2020 - Secondary Containment was declared inoperable due to a rise in differential pressure.
This was reported under LER 2020-004-00 as a loss of safety function under 10 CFR 50.73(a)(2)(v)(C and D) -
An event or condition that have could have prevented the fulfillment of the safety function of structures or systems that are needed to control the release of radioactive material or mitigate the consequences of an accident.
On August 6, 2020 - Secondary Containment was declared inoperable due to a rise in differential pressure.
This was reported under LER 2020-002-00 as a loss of safety function under 10 CFR 50. 73(a)(2)(v)(C and D) -
An event or condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to control the release of radioactive material or mitigate the consequences of an accident.
On May 1, 2020 - Secondary Containment was breached due to both airlock doors in the Reactor Building being inadvertently open simultaneously. This was reported under LER 2020-001-00 as a loss of safety function under 10 CFR 50.73(a)(2)(v)(C and D) -An event or condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to control the release of radioactive material or mitigate the consequences of an accident.
On August 8, 2019 - Secondary Containment was declared inoperable due to a rise in differential pressure.
This was reported under LER 2019-002-00 as a loss of safety function under 10 CFR 50. 73(a)(2)(v)(C and D) -
An event or condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to control the release of radioactive material or mitigate the consequences of an accident.
On January 6, 2014 - Secondary Containment was declared inoperable due to a rise in differential pressure.
This was reported under LER 2014-001-00 as a loss of safety function under 10 CFR 50. 73(a)(2)(v)(C and D) -
An event or condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to control the release of radioactive material or mitigate the consequences of an accident.