ML17347A650: Difference between revisions

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| issue date = 12/11/1987
| issue date = 12/11/1987
| title = Forwards JPE-PTPO-87-350, Outside Containment Limitorque Wire Rept, as Committed to in Util 860829 Ltr.Rept Concludes That Limitorque Operators Would Have Performed Designed Safety Function
| title = Forwards JPE-PTPO-87-350, Outside Containment Limitorque Wire Rept, as Committed to in Util 860829 Ltr.Rept Concludes That Limitorque Operators Would Have Performed Designed Safety Function
| author name = WOODY C O
| author name = Woody C
| author affiliation = FLORIDA POWER & LIGHT CO.
| author affiliation = FLORIDA POWER & LIGHT CO.
| addressee name =  
| addressee name =  
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=Text=
=Text=
{{#Wiki_filter:REGULAY INPORNATION DISTRIBUTI(SYBTEN (RIDE>4 ACOI=SSION NBR: 8712140438 DOC.DATE: 87/12/11 NOTARIZED:
{{#Wiki_filter:REGULAY     INPORNATION DISTRIBUTI(SYBTEN     (RIDE>
NO FACIL: 50-250 Turkey Point Planti Unit 3i Florida Power and Light C 50-251 Turkey Point Planti Unit 44 Florida Power and Light C AUTH.NAME AUTHOR AFFILIATION WOODY4 C.O.Florida Power 8c Light Co.RECIP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)DOCKET 5 05000250 05000251
4 ACOI=SSION NBR: 8712140438     DOC. DATE: 87/12/11   NOTARIZED: NO         DOCKET 5 FACIL: 50-250 Turkey Point   Planti Unit 3i Florida Power and Light C 05000250 50-251 Turkey Point   Planti Unit 44 Florida Power and Light C 05000251 AUTH. NAME           AUTHOR AFFILIATION WOODY4 C. O.         Florida Power 8c Light Co.
RECIP. NAME         RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)


==SUBJECT:==
==SUBJECT:==
Forwards outside containment limitorque wire rept.Evaluation concludes that Limitorque operators would have perFormed designed safety function had operators been called upon to do so.N/o encls to evaluation.
Forwards     outside containment limitorque wire rept.
DISTRIBUTION CODE:*04BD COPIES RECEIVED;LTR i ENCL Q SIZE I+I TITLE: OR/Licensing Submittal:
Evaluation concludes that Limitorque operators would have perFormed designed safety function had operators been called upon to do so. N/o encls to evaluation.
Equipment Qualification NOTES: RECIPIENT ID CODE/NAME PD2-2 LA McDONALDB D INTERNAL: ARM/DAF/LFMB NRR/DEST/ADE NRR/DEST/SQB C IL 01 EXTERNAL: LPDR NSIC COPIES LTTR ENCL 1 0 1 1 1 0 1 0 1 1 1 1 1 1 RECIPIENT ID CODE/NAME PD2-2 PD QC NRR/DEBT/MEB OQC/HDS2 RES/DE/E I 8 NRC PDR COPIES LTTR ENCL 1 0 1 1 1 1 1 1 1 1 TOTAL NUMBER OF COPIES'EQUIRED:
DISTRIBUTION CODE: *04BD     COPIES RECEIVED; LTR   i   ENCL Q SIZE   I + I TITLE: OR/Licensing Submittal: Equipment Qualification NOTES:
LTTR 14 ENCL 10 t t (*P)I l P.O.14000, JUNO BEACH, FL 3340S-0420
RECIPIENT        COPIES            RECIPIENT       COPIES ID CODE/NAME     LTTR ENCL        ID CODE/NAME    LTTR ENCL PD2-2 LA             1    0      PD2-2 PD            1    0 McDONALDB D           1    1 INTERNAL: ARM/DAF/LFMB           1    0      QC                  1    1 NRR/DEST/ADE         1    0      NRR/DEBT/MEB        1     1 NRR/DEST/SQB          1    1      OQC/HDS2             1    1 IL      01          1      RES/DE/E I 8         1     1 C
+i/(I<~>>DECEMBER 1 1 3987 L-87-499 U.S.Nuclear Regulatory Commission Attn: Document Control Desk Washington, D.C.20555 Gentlemen:
EXTERNAL: LPDR                          1     NRC PDR NSIC                  1     1 TOTAL NUMBER OF COPIES'EQUIRED:       LTTR   14   ENCL     10
Re: Turkey Point Units 3 and 4 Docket Nos.50-250 and 50-251 Limitorque Valve Wiring Qualifications Unresolved Item 86-39-06 Our letter dated August 29, 1986 discussed the discovery of some wiring in Limitorque motor operated valves outside the containment which were on the environmental qualification list that may not have been fully supported by available documentation.
 
In that letter we stated we would submit the results of our analysis of the as-found condition.
t t
The attached evaluation concludes that the Limitorque operators would have performed their designed safety function had they been called upon to do so.Due to the size of the full report, the attachments to the evaluation have not been included but are available on site for your review.Very truly yours, O.Woody Executive Vice President COW/SDF/cn:
(
M:006 Attachment cc: Dr.J.Nelson Grace, Regional Administrator, Region II, USNRC Senior Resident Inspector, USNRC, Turkey Point Plant 8712140438 871211 Q PDR ADDCK 05000250 p PDRQ~4 p0 PEOPLE...SERVING PEOPLE}}
* P
    )
I l
 
P. O. 14000, JUNO BEACH, FL 3340S-0420
                                                                                            +i/(I<~>>
DECEMBER 1 1 3987 L-87-499 U.S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, D.C. 20555 Gentlemen:
Re:   Turkey Point Units 3 and 4 Docket Nos. 50-250 and 50-251 Limitorque Valve Wiring Qualifications Unresolved Item 86-39-06 Our letter dated August 29, 1986 discussed the discovery of some wiring in Limitorque motor operated valves outside the containment which were on the environmental qualification list that may not have been fully supported by available documentation. In that letter we stated we would submit the results of our analysis of the as-found condition.
The attached     evaluation concludes that the Limitorque operators would have performed their designed     safety function had they been called upon to do so.
Due to the size of the       full report, the attachments to the evaluation have not been included but are   available on site for your review.
Very truly yours, O. Woody Executive Vice President COW/SDF/cn: M:006 Attachment cc:   Dr. J. Nelson Grace, Regional Administrator, Region II, USNRC Senior Resident Inspector, USNRC, Turkey Point Plant 8712140438 871211 Q                                                                                   ~4 PDR   ADDCK 05000250 p                   PDRQ p0 PEOPLE... SERVING PEOPLE}}

Latest revision as of 09:27, 22 October 2019

Forwards JPE-PTPO-87-350, Outside Containment Limitorque Wire Rept, as Committed to in Util 860829 Ltr.Rept Concludes That Limitorque Operators Would Have Performed Designed Safety Function
ML17347A650
Person / Time
Site: Turkey Point  NextEra Energy icon.png
Issue date: 12/11/1987
From: Woody C
FLORIDA POWER & LIGHT CO.
To:
NRC OFFICE OF ADMINISTRATION & RESOURCES MANAGEMENT (ARM)
Shared Package
ML17347A651 List:
References
L-87-499, NUDOCS 8712140438
Download: ML17347A650 (4)


Text

REGULAY INPORNATION DISTRIBUTI(SYBTEN (RIDE>

4 ACOI=SSION NBR: 8712140438 DOC. DATE: 87/12/11 NOTARIZED: NO DOCKET 5 FACIL: 50-250 Turkey Point Planti Unit 3i Florida Power and Light C 05000250 50-251 Turkey Point Planti Unit 44 Florida Power and Light C 05000251 AUTH. NAME AUTHOR AFFILIATION WOODY4 C. O. Florida Power 8c Light Co.

RECIP. NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)

SUBJECT:

Forwards outside containment limitorque wire rept.

Evaluation concludes that Limitorque operators would have perFormed designed safety function had operators been called upon to do so. N/o encls to evaluation.

DISTRIBUTION CODE: *04BD COPIES RECEIVED; LTR i ENCL Q SIZE I + I TITLE: OR/Licensing Submittal: Equipment Qualification NOTES:

RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD2-2 LA 1 0 PD2-2 PD 1 0 McDONALDB D 1 1 INTERNAL: ARM/DAF/LFMB 1 0 QC 1 1 NRR/DEST/ADE 1 0 NRR/DEBT/MEB 1 1 NRR/DEST/SQB 1 1 OQC/HDS2 1 1 IL 01 1 RES/DE/E I 8 1 1 C

EXTERNAL: LPDR 1 NRC PDR NSIC 1 1 TOTAL NUMBER OF COPIES'EQUIRED: LTTR 14 ENCL 10

t t

(

  • P

)

I l

P. O. 14000, JUNO BEACH, FL 3340S-0420

+i/(I<~>>

DECEMBER 1 1 3987 L-87-499 U.S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, D.C. 20555 Gentlemen:

Re: Turkey Point Units 3 and 4 Docket Nos. 50-250 and 50-251 Limitorque Valve Wiring Qualifications Unresolved Item 86-39-06 Our letter dated August 29, 1986 discussed the discovery of some wiring in Limitorque motor operated valves outside the containment which were on the environmental qualification list that may not have been fully supported by available documentation. In that letter we stated we would submit the results of our analysis of the as-found condition.

The attached evaluation concludes that the Limitorque operators would have performed their designed safety function had they been called upon to do so.

Due to the size of the full report, the attachments to the evaluation have not been included but are available on site for your review.

Very truly yours, O. Woody Executive Vice President COW/SDF/cn: M:006 Attachment cc: Dr. J. Nelson Grace, Regional Administrator, Region II, USNRC Senior Resident Inspector, USNRC, Turkey Point Plant 8712140438 871211 Q ~4 PDR ADDCK 05000250 p PDRQ p0 PEOPLE... SERVING PEOPLE