IR 05000334/2009003: Difference between revisions

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{{Adams|number = ML092160021}}
{{Adams
| number = ML092160021
| issue date = 08/04/2009
| title = IR 05000334-09-003 & 05000412-09-003 on 04/01/09 - 06/30/09 for Beaver Valley
| author name = Bellamy R R
| author affiliation = NRC/RGN-I/DRP/PB6
| addressee name = Sena P P
| addressee affiliation = FirstEnergy Nuclear Operating Co
| docket = 05000334, 05000412
| license number = DPR-066, NPF-073
| contact person = BELLAMY RR
| document report number = IR-09-003
| document type = Inspection Report, Letter
| page count = 42
}}


{{IR-Nav| site = 05000334 | year = 2009 | report number = 003 }}
{{IR-Nav| site = 05000334 | year = 2009 | report number = 003 }}


=Text=
=Text=
{{#Wiki_filter:
{{#Wiki_filter:UNITED STATES  NUCLEAR REGULATORY COMMISSION    REGION I 475 ALLENDALE ROAD  KING OF PRUSSIA, PA 19406-1415 August 4, 2009  
[[Issue date::August 4, 2009]]


Mr. Peter P. Sena, III Site Vice President FirstEnergy Nuclear Operating Company Beaver Valley Power Station P. O. Box 4, Route 168 Shippingport, PA 15077
Mr. Peter P. Sena, III Site Vice President FirstEnergy Nuclear Operating Company Beaver Valley Power Station P. O. Box 4, Route 168 Shippingport, PA 15077
Line 21: Line 34:
consistent with Section VI.A.1 of the NRC Enforcement Policy. If you contest any of the findings in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator Region I; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at Beaver Valley. In addition, if you disagree with the characterization of the cross-cutting aspect of any finding in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region 1 and the NRC Senior Resident Inspector at the Beaver Valley Power Station.
consistent with Section VI.A.1 of the NRC Enforcement Policy. If you contest any of the findings in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator Region I; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at Beaver Valley. In addition, if you disagree with the characterization of the cross-cutting aspect of any finding in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region 1 and the NRC Senior Resident Inspector at the Beaver Valley Power Station.


In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, and its enclosures, and your response (if any) will be available electronically for public inspection in the P. Sena, III 2 NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Website at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, and its enclosures, and your response (if any) will be available electronically for public ins pection in the P. Sena, III 2  
 
NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Website at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).


We appreciate your cooperation. Please contact me at 610-337-5200 if you have any questions regarding this letter.
We appreciate your cooperation. Please contact me at 610-337-5200 if you have any questions regarding this letter.
Line 35: Line 50:
===w/Attachment:===
===w/Attachment:===
Supplemental Information cc w/encl:
Supplemental Information cc w/encl:
J. Hagan, President and Chief Nuclear Officer J. Lash, Senior Vice President of Operations and Chief Operating Officer D. Pace, Senior Vice President, Fleet Engineering K. Fili, Vice President, Fleet Oversight P. Harden, Vice President, Nuclear Support G. Halnon, Director, Fleet Regulatory Affairs Manager, Fleet Licensing Company R. Lieb, Director, Site Operations D. Murray, Director, Maintenance M. Manoleras, Director, Engineering R. Brosi, Director, Site Performance Improvement C. Keller, Manager, Site Regulatory Compliance D. Jenkins, Attorney, FirstEnergy Corporation M. Clancy, Mayor, Shippingport, PA D. Allard, Director, PADEP C. O'Claire, State Liaison to the NRC, State of Ohio Z. Clayton, EPA-DERR, State of Ohio Director, Utilities Department, Public Utilities Commission, State of Ohio D. Hill, Chief, Radiological Health Program, State of West Virginia J. Lewis, Commissioner, Division of Labor, State of West Virginia W. Hill, Beaver County Emergency Management Agency J. Johnsrud, National Energy Committee, Sierra Club P. Sena, III 3 NRC's document system (ADAMS). ADAMS is accessible from the NRC Website at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
J. Hagan, President and Chief Nuclear Officer J. Lash, Senior Vice President of Operations and Chief Operating Officer D. Pace, Senior Vice President, Fleet Engineering  
 
K. Fili, Vice President, Fleet Oversight P. Harden, Vice President, Nuclear Support G. Halnon, Director, Fleet Regulatory Affairs Manager, Fleet Licensing Company R. Lieb, Director, Site Operations D. Murray, Director, Maintenance M. Manoleras, Director, Engineering R. Brosi, Director, Site Performance Improvement C. Keller, Manager, Site Regulatory Compliance D. Jenkins, Attorney, FirstEnergy Corporation M. Clancy, Mayor, Shippingport, PA D. Allard, Director, PADEP C. O'Claire, State Liaison to the NRC, State of Ohio Z. Clayton, EPA-DERR, State of Ohio  
 
Director, Utilities Department, Public Utilities Commission, State of Ohio D. Hill, Chief, Radiological Health Program, State of West Virginia J. Lewis, Commissioner, Division of Labor, State of West Virginia W. Hill, Beaver County Emergency Management Agency J. Johnsrud, National Energy Committee, Sierra Club P. Sena, III 3  
 
NRC's document system (ADAMS). ADAMS is accessible from the NRC Website at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).


We appreciate your cooperation. Please contact me at 610-337-5200 if you have any questions regarding this letter.
We appreciate your cooperation. Please contact me at 610-337-5200 if you have any questions regarding this letter.
Line 41: Line 62:
Sincerely,/RA/ Ronald R. Bellamy, Ph.D., Chief Reactor Projects Branch 6 Division of Reactor Projects  
Sincerely,/RA/ Ronald R. Bellamy, Ph.D., Chief Reactor Projects Branch 6 Division of Reactor Projects  


Distribution w/encl: S. Collins, RA M. Dapas, DRA D. Lew, DRP J. Clifford, DRP R. Bellamy, DRP G. Barber, DRP C. Newport, DRP J. Greives, DRP D. Werkheiser, DRP, SRI D. Spindler, DRP, RI P. Garrett, DRP, Resident OA L. Trocine, RI OEDO R. Nelson, NRR N. Morgan, PM, NRR R. Guzman, NRR S. West, DRS-RIII C. Pederson, DRP-RIII ROPreportsResource@nrc.gov Region I Docket Room (with concurrences)
Distribution w/encl
: S. Collins, RA M. Dapas, DRA D. Lew, DRP J. Clifford, DRP R. Bellamy, DRP G. Barber, DRP C. Newport, DRP J. Greives, DRP D. Werkheiser, DRP, SRI D. Spindler, DRP, RI P. Garrett, DRP, Resident OA L. Trocine, RI OEDO R. Nelson, NRR N. Morgan, PM, NRR R. Guzman, NRR S. West, DRS-RIII  


ML092160021 SUNSI Review Complete: RRB (Reviewer's Initials) DOCUMENT NAME: G:\DRP\BRANCH6\+++BEAVER VALLEY\BV INSPECTION REPORTS & EXIT NOTES\ BV INSPECTION REPORTS 2009\BVREPORT-IR2009-003.DOC After declaring this document "An Official Agency Record" it will be released to the Public . To receive a copy of this document, indicate in the box: "C" = Copy without attachment/enclosure "E" = Copy with attachment/enclosure "N" = No copy OFFICE RI/DRP RI/DRP NAME DWerkheiser/DW RBellamy/ RRB DATE 07/29/09 08/04/09 OFFICIAL RECORD COPY 1 Enclosure U. S. NUCLEAR REGULATORY COMMISSION REGION I  
C. Pederson, DRP-RIII ROPreportsResource@nrc.gov Region I Docket Room (with concurrences)
 
ML092160021 SUNSI Review Complete: RRB (Reviewer's Initials)
DOCUMENT NAME: G:\DRP\BRANCH6\+++BEAVER VALLEY\BV INSPECTION REPORTS & EXIT NOTES\ BV INSPECTION REPORTS 2009\BVREPORT-IR2009-003.DOC After declaring this document "An Official Agency Record" it will be released to the Public . To receive a copy of this document, indicate in the box:  
" C" = Copy without attachment/enclosure " E" = Copy with attachment/enclosure " N" = No copy OFFICE RI/DRP RI/DRP NAME DWerkheiser/DW RBellamy/ RRB DATE 07/29/09 08/04/09 OFFICIAL RECORD COPY 1 Enclosure U. S. NUCLEAR REGULATORY COMMISSION REGION I  


Docket Nos. 50-334, 50-412  
Docket Nos. 50-334, 50-412  
Line 59: Line 85:
Dates: April 1, 2009 through June 30, 2009  
Dates: April 1, 2009 through June 30, 2009  


Inspectors: D. Werkheiser, Senior Resident Inspector D. Spindler, Resident Inspector J. Ayala, Resident Inspector P. Kaufman, Senior Reactor Inspector T. Moslak, Health Physicist O. Ayegbusi, Reactor Inspector Approved by: R. Bellamy, Ph.D., Chief Reactor Projects Branch 6 Division of Reactor Projects  
Inspectors: D. Werkheiser, Senior Resident Inspector D. Spindler, Resident Inspector J. Ayala, Resident Inspector P. Kaufman, Senior Reactor Inspector T. Moslak, Health Physicist O. Ayegbusi, Reactor Inspector  
 
Approved by: R. Bellamy, Ph.D., Chief Reactor Projects Branch 6 Division of Reactor Projects  


2 Enclosure TABLE of  
2 Enclosure TABLE of  


=SUMMARY OF FINDINGS=
=SUMMARY OF FINDINGS=
.............................................................................................................. 3
IR 05000334/2009003, IR 05000412/2009003; 04/01/2009 - 06/30/2009; Beaver Valley Power
 
Station, Units 1 & 2; Post-Maintenance Testing, Problem Identification and Resolution
 
The report covered a 3-month period of inspection by resident inspectors, regional reactor inspectors, and a regional health physics inspector. Two (GREEN) findings were identified. The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, ASignificance Determination Process
@ (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. Cross-cutting aspects associated with findings are determined using IMC 0305, "Operating Reactor Assessment Program," dated January 2009. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, AReactor Oversight Process,@ Revision 4, dated December 2006.
 
===Cornerstone: Mitigating Systems===
: '''Green.'''
A non-cited violation (NCV) of 10CFR Part 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings" was identified for failure to specify and perform an adequate post-maintenance test (PMT) after replacing a safety-related river water check-valve. Specifically, the PMT under work order 200233562 was not adequate to verify the proper function of the valve 1RW-57 prior to its return to service. The PMT was subsequently performed successfully. This issue was entered into the licensee's corrective action program as condition report 09-59866.
 
The failure to specify and perform an adequate PMT after replacing a safety-related river water check-valve was a performance deficiency. The finding was more than minor in accordance with IMC 0612, Appendix B (Section 1-3), "Issue Screening," because the failure to specify and perform an adequate PMT is associated with the procedure quality performance attribute of the mitigating systems cornerstone and affects the associated cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences.
 
This finding has a cross-cutting aspect in the area of human performance associated with resources because the licensee did not have complete, accurate, and up-to-date maintenance work procedures [IMC 0305 Aspect:
H.2(c)] (Section 1R19).
: '''Green.'''
The inspectors identified a non-cited violation (NCV) of 10CFR Part 50, Appendix B, Crit erion III, "Design Control," in that FENOC failed to maintain safety-related cables in an environment for which they were designed. Since NRC Information Notice 2002-12 was issued, FENOC has had several opportunities to trend as-found data, implement effective maintenance programs, and identify and thoroughly evaluate long-term adverse conditions for underground safety-related cables exposed to continuous submerged environments. Cables affected include those for Unit 1 river water and Unit 2 service water. The issue was entered into the licensee's corrective action program (CR 09-60496) to initiate a review of the current manhole and cable monitoring programs, and to initiate long-term corrective actions.
 
Failure to maintain safety related cables in an environment for which they were designed is considered a performance deficiency. The finding was more than minor in accordance with IMC 0612, Appendix B (Section 1-3), "Issue Screening," because if left uncorrected, the performance deficiency has the potential to lead to a more significant safety concern.
 
Specifically, the deficiency did not result in the present loss of operability or functionality and did not represent a risk significant external event such as flooding. The issue was entered into the licensee's corrective action program (CR 09-60496) to initiate a review of the current manhole and cable monitoring programs, and to initiate long-term corrective actions.
 
The performance deficiency had a cross-cutting aspect in the area of Problem Identification and Resolution, Corrective Action Program, because the licensee did not thoroughly evaluate problems such as resolutions, address causes, and evaluate the effectiveness of corrective actions [IMC 0305 Aspect:
P.1 (c)] (Section 4OA2.3).
 
===Other Findings===
A violation of very low safety significance, which was identified by the licensee, has been reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensee's corrective action program. This violation and corrective actions are listed in Section 4OA7 of this report.


=REPORT DETAILS=
=REPORT DETAILS=
..........................................................................................................................
 
===Summary of Plant Status===
:  Unit 1 began the inspection period at 100 percent power. On April 1, the unit began a planned coastdown, on April 16 reduced power to 82 percent for planned condenser waterbox cleaning, and shut down on April 19 to commence a refueling outage (1R19).
 
On May 21, the unit was restarted and synchronized to the grid, achieving full power on May 24. The unit remained at 100 percent power for the remainder of the inspection period.
 
Unit 2 began the inspection period at 100 percent power. On April 18, the unit was down-powered to 97 percent for planned turbine valve testing and returned to full power later the same day. On May 30 through May 31 the unit was reduced to 96 percent to address first-point feedwater heater level control issues and returned to full power. The unit remained at 100 percent power for the remainder of the inspection period.
 
1.


==REACTOR SAFETY==
==REACTOR SAFETY==
............................................................................................................ 5 1R01 Adverse Weather Protection ) ..................................................................................... 5 1R04 Equipment Alignment  ................................................................................................. 6 1R05 Fire Protection  ............................................................................................................ 7    1R06      Flood Protection Measures .......................................................................................... 8 1R08      Unit 1 Inservice Inspection  .......................................................................................... 8    1R11        Licensed Operator Requalification Program ............................................................ 11 1R12 Maintenance Rule Implementation  ........................................................................... 11 1R13  Maintenance Risk Assessment and Emergent Work Control  .................................. 12 1R15 Operability Evaluations  ............................................................................................. 12 1R18  Plant Modifications  .................................................................................................... 13 1R19 Post-Maintenance Testing  ........................................................................................ 14 1R20 Refueling and Outage Activities  ............................................................................... 16 1R22  Surveillance Testing


==RADIATION SAFETY==
===Cornerstone:===
............................................................................................................... 17 2OS1 Access Control to Radiologically Significant Areas  .................................................. 17 2OS2 ALARA Planning and Controls
Initiating Events, Mitigating Systems, Barrier Integrity [R]
{{a|1R01}}
==1R01 Adverse Weather Protection==
{{IP sample|IP=IP 71111.01}}
===.1 Seasonal Susceptibility===
 
====a. Inspection Scope====
(2 samples - Hot Weather / Hurricane, Offsite and Alternate AC Power System Readiness)
The inspectors reviewed the Beaver Valley Power Station (BVPS) design features and FENOC's implementation of procedures to protect risk significant mitigating systems from adverse weather effects due to summer weather and hurricanes. The inspectors conducted interviews with various station personnel to gain insights into the station's hot weather and hurricane readiness and reviewed the status of various work orders categorized as warm weather preparation activities. The inspectors reviewed the corrective action program database, operating experience, and the Updated Final Safety Analysis Report (UFSAR), to determine the types of adverse weather conditions to which the site is susceptible, and to verify that the licensee was appropriately identifying and resolving weather-rela ted equipment problems.
 
The inspectors also reviewed BVPS design features and FENOC's implementation of procedures to handle issues that could impact offsite and alternating current (AC) power systems. The inspectors reviewed FENOC's procedures and programs which discussed
 
the operation and availability/reliability of offsite and alternate AC power sy stems during adverse weather. The inspectors verified that communication protocols between the transmission system operator and FENOC existed, and the appropriate information would be conveyed when potential grid stress and disturbances existed. The inspectors also verified that FENOC's procedures contained actions to monitor and maintain the availability/reliability of offsite and onsite power systems prior to and during adverse weather conditions.
 
====b. Findings====
No findings of significance were identified.
{{a|1R04}}
==1R04 Equipment Alignment==
{{IP sample|IP=IP 71111.04}}
===.1 Partial System Walkdowns===
{{IP sample|IP=IP 71111.04Q}}
 
====a. Inspection Scope====
(4 samples)
The inspectors performed four partial equipment alignment inspections during conditions of increased safety significance, including when redundant equipment was unavailable during maintenance or adverse conditions. The partial alignment inspections were also completed after equipment was recently returned to service after significant maintenance. The inspectors performed partial walkdowns of the following systems, including associated electrical distribution components and control room panels, to verify the equipment was aligned to perform its intended safety functions:
* Unit 1, on April 14, emergency diesel generator No. 1 during the performance of 1OST-36.2, "Diesel Generator No. 2 Monthly Test;"
* Unit 1, on April 16, train 'A' high head safety injection during the performance of 1OST-7.19D, "Safety Injection Relay Test (Slave Relay K610)-Train B;"
* Unit 1, on April 21, train 'B' residual heat removal system while 'A' electrical train was cleared for maintenance; and
* Unit 1, on April 29, containment penetrations during the core reload.
 
====b. Findings====
No findings of significance were identified.
 
===.2 Complete System Walkdown===
{{IP sample|IP=IP 71111.04S}}
 
====a. Inspection Scope====
(2 samples)
The inspectors performed complete system walkdowns of the following systems to verify that the critical portions, such as valve positions, switches, and breakers, were correctly aligned in accordance with procedures, and to identify any discrepancies that may have had an effect on operability.
 
The inspectors also reviewed outstanding maintenance work orders to verify that the deficiencies did not significantly affect the system function. In addition, the inspectors discussed system health with the system engineer and reviewed the condition report database to verify that equipment alignment problems were being identified and appropriately resolved. Documents reviewed during the inspection are listed in the
.
* On June 4, alignment and condition of the Unit 2 'C' service water pump and 'A' service water train while the 'D' main intake bay (affecting the 'A' service water pump) was out of service for planned cleaning; and
* On June 6, alignment of 'A' and 'B' motor-driven auxiliary and dedicated feedwater pumps while the turbine-driven feedwater pump was out of service for planned maintenance.
 
====b. Findings====
No findings of significance were identified.
{{a|1R05}}
==1R05 Fire Protection==
{{IP sample|IP=IP 71111.05}}
===.1 Quarterly Sample Review===
{{IP sample|IP=IP 71111.05Q}}
 
====a. Inspection Scope====
(7 samples)
The inspectors reviewed the conditions of the fire areas listed below, to verify compliance with criteria delineated in Administrative Procedure 1/2-ADM-1900, "Fire Protection,"
Rev. 19. This review included FENOC's control of transient combustibles and ignition sources, material condition of fire protection equipment including fire detection systems, water-based fire suppression systems, gaseous fire suppression systems, manual firefighting equipment and capability, passive fire protection features, and the adequacy of compensatory measures for any fire protection impairments. Documents reviewed are listed in the Attachment:
* Unit 2, TR-MT-2 Main Transformer (Fire Area TR-1);
* Unit 2, TR-2C Unit Station Service Transformer (Fire Area TR-2);
* Unit 2, TR-2D Unit Station Service Transformer (Fire Area TR-3);
* Unit 1, AE Switchgear Room, Battery Rooms 1& 3 (Fire Area ES-1);
* Unit 1, DF Switchgear Room, Battery Rooms 2& 4 (Fire Area ES-2);
* Unit 1, Reactor Containment (Fire Area RC-1); and
* Unit 1, Rod Control Motor Generator Room (Fire Area MG-1)


==OTHER ACTIVITIES==
====b. Findings====
[OA] ..................................................................................................... 21
No findings of significance were identified.
{{a|4OA1}}
==4OA1 Performance Indicator Verification==
  ........................................................................... 21
{{a|4OA2}}
==4OA2 Problem Identification and Resolution==
  ...................................................................... 22
{{a|4OA3}}
==4OA3 Followup of Events and Notices of Enforcement Discretion==
  .................................... 25
{{a|4OA5}}
==4OA5 Other Activities ........................................................................................................... 26 4OA6 Meetings, Including Exit ............................................................................................. 27 4OA7 Licensee-Identified Violations .................................................................................... 28==


=SUPPLEMENTAL INFORMATION=
===.2 Annual Fire Drill Observation===
{{IP sample|IP=IP 71111.05A}}


==KEY POINTS OF CONTACT==
====a. Inspection Scope====
...................................................................................................... A-1
(1 sample)
==LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED==
The inspectors observed personnel performance during response to an indicated fire in the Emergency Response Facility sub-stat ion (also see Section 40A3.1) by the fire brigade on June 18. The inspection evaluated the station's demonstration of readiness in fire fighting response. The inspectors observed the fire brigade members using protective clothing, turnout gear, and self-contained breathing apparatus and entering the fire area in a controlled manner. The inspectors also observed the fire fighting equipment brought to the fire scene to evaluate whether sufficient equipment was available to effectively control and extinguish the simulated fire. The inspectors evaluated whether the permanent plant fire hose lines were capable of reaching the fire area and whether hose usage was adequate. The inspectors observed the fire fighting directions and communications between fire brigade members. The inspectors verified that the pre-fire plan was used and observed the post-event critique to evaluate fact-finding, lessons-learned and whether any immediate deficiencies needed addressed.
.......................................................... A-1  
==LIST OF DOCUMENTS REVIEWED==
.......................................................................................... A-2
==LIST OF ACRONYMS==
............................................................................................................... A-10
Enclosure
: [[SUMMAR]] [[Y]]
: [[OF]] [[]]
: [[FINDIN]] [[]]
: [[GS]] [[]]
: [[IR]] [[05000334/2009003,]]
IR 05000412/2009003; 04/01/2009 - 06/30/2009; Beaver Valley Power
Station, Units 1 & 2; Post-Maintenance Testing, Problem Identification and Resolution


The report covered a 3-month period of inspection by resident inspectors, regional reactor
====b. Findings====
inspectors, and a regional health physics inspector. Two (GREEN) findings were identified. The
No findings of significance were identified.
significance of most findings is indicated by their color (Green, White, Yellow, Red) using
{{a|1R06}}
Inspection Manual Chapter (IMC) 0609,
==1R06 Flood Protection Measures==
: [[AS]] [[ignificance Determination Process@ (]]
{{IP sample|IP=IP 71111.06}}
: [[SDP]] [[). Findings for which the]]
: [[SDP]] [[does not apply may be Green or be assigned a severity level after]]
NRC management review. Cross-cutting aspects associated with findings are determined using IMC
0305, "Operating Reactor Assessment Program," dated January 2009. The NRC's program for
overseeing the safe operation of commercial nuclear power reactors is described in
: [[NUR]] [[]]
EG-
1649,
: [[AR]] [[eactor Oversight Process,@ Revision 4, dated December 2006. Cornerstone: Mitigating Systems  * Green. A non-cited violation (]]
NCV) of 10CFR Part 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings" was identified for failure to specify and perform
an adequate post-maintenance test (PMT) after replacing a safety-related river water
check-valve. Specifically, the PMT under work order 200233562 was not adequate to
verify the proper function of the valve
: [[1RW]] [[-57 prior to its return to service. The]]
PMT was
subsequently performed successfully. This issue was entered into the licensee's
corrective action program as condition report 09-59866. The failure to specify and perform an adequate PMT after replacing a safety-related river
water check-valve was a performance deficiency. The finding was more than minor in
accordance with IMC 0612, Appendix B (Section 1-3), "Issue Screening," because the
failure to specify and perform an adequate PMT is associated with the procedure quality
performance attribute of the mitigating systems cornerstone and affects the associated
cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences.  


This finding has a cross-cutting aspect in the area of human performance associated
====a. Inspection Scope====
with resources because the licensee did not have complete, accurate, and up-to-date
(1 sample - underground cables)
maintenance work procedures [IMC 0305 Aspect:
The inspectors reviewed a sample of internal flood protection measures regarding cables located in underground manholes. The inspectors selected a FENOC inspection of manholes 8A and 8B that contain Unit 1 and Unit 2 safety-related power and control cables near the main intake structure. These cable manholes are underground and also the focus of a focus problem identification and resolution review (see section 4OA2.3).
: [[H.]] [[2(c)] (Section 1R19).  * Green. The inspectors identified a non-cited violation (]]
: [[NCV]] [[) of]]
: [[10CFR]] [[Part 50, Appendix B, Criterion]]
: [[III]] [[, "Design Control," in that]]
: [[FENOC]] [[failed to maintain safety-related cables in an environment for which they were designed. Since]]
NRC Information
Notice 2002-12 was issued,
: [[FEN]] [[]]
OC has had several opportunities to trend as-found
data, implement effective maintenance programs, and identify and thoroughly evaluate
long-term adverse conditions for underground safety-related cables exposed to
continuous submerged environments. Cables affected include those for Unit 1 river
water and Unit 2 service water. The issue was entered into the licensee's corrective
action program (CR 09-60496) to initiate a review of the current manhole and cable
monitoring programs, and to initiate long-term corrective actions.  


Enclosure Failure to maintain safety related cables in an environment for which they were designed is considered a performance deficiency. The finding was more than minor in accordance
This review was conducted to evaluate FENOC's protection of the enclosed safety-related systems from internal flooding condition. The inspectors entered the confined area with FENOC personnel, inspected the manhole, and monitored licensee maintenance activities. The inspectors also reviewed the UFSAR, related internal flooding evaluations, and other related documents. The inspectors examined the as-found equipment and conditions to ensure that they remained consistent with those indicated in the design basis documentation, flooding mitigation documents, and risk analysis assumptions. Documents reviewed during the inspection are listed in the  
with IMC 0612, Appendix B (Section 1-3), "Issue Screening," because if left uncorrected,
.
the performance deficiency has the potential to lead to a more significant safety concern.
Specifically, the deficiency did not result in the present loss of operability or functionality and did not represent a risk significant external event such as flooding. The issue was
entered into the licensee's corrective action program (CR 09-60496) to initiate a review of
the current manhole and cable monitoring programs, and to initiate long-term corrective
actions.  


The performance deficiency had a cross-cutting aspect in the area of Problem
====b. Findings====
Identification and Resolution, Corrective Action Program, because the licensee did not
One finding of significance was identified and documented in section 4OA2.3.
thoroughly evaluate problems such as resolutions, address causes, and evaluate the
{{a|1R08}}
effectiveness of corrective actions [IMC 0305 Aspect:
==1R08 Unit 1 Inservice Inspection (IP 71111.08)==
: [[P.]] [[1 (c)] (Section 4]]
OA2.3). Other Findings  A violation of very low safety significance, which was identified by the licensee, has been
reviewed by the inspectors. Corrective actions taken or planned by the licensee have
been entered into the licensee's corrective action program. This violation and corrective
actions are listed in Section 4OA7 of this report.
Enclosure
: [[REPORT]] [[]]
DETAILS  Summary of Plant Status:  Unit 1 began the inspection period at 100 percent power. On April 1, the unit began a
planned coastdown, on April 16 reduced power to 82 percent for planned condenser
waterbox cleaning, and shut down on April 19 to commence a refueling outage (1R19).
On May 21, the unit was restarted and synchronized to the grid, achieving full power on
May 24. The unit remained at 100 percent power for the remainder of the inspection
period. Unit 2 began the inspection period at 100 percent power. On April 18, the unit was
down-powered to 97 percent for planned turbine valve testing and returned to full power
later the same day. On May 30 through May 31 the unit was reduced to 96 percent to
address first-point feedwater heater level control issues and returned to full power. The
unit remained at 100 percent power for the remainder of the inspection period.
1.
: [[REACTO]] [[R]]
SAFETY  Cornerstone: Initiating Events, Mitigating Systems, Barrier Integrity [R]
1R01 Adverse Weather Protection (71111.01) 
.1 Seasonal Susceptibility
a. Inspection Scope (2 samples - Hot Weather / Hurricane, Offsite and Alternate
: [[AC]] [[Power System Readiness)  The inspectors reviewed the Beaver Valley Power Station (]]
: [[BVPS]] [[) design features and]]
: [[FEN]] [[]]
OC's implementation of procedures to protect risk significant mitigating systems from
adverse weather effects due to summer weather and hurricanes. The inspectors
conducted interviews with various station personnel to gain insights into the station's hot
weather and hurricane readiness and reviewed the status of various work orders
categorized as warm weather preparation activities. The inspectors reviewed the
corrective action program database, operating experience, and the Updated Final Safety
Analysis Report (UFSAR), to determine the types of adverse weather conditions to which
the site is susceptible, and to verify that the licensee was appropriately identifying and
resolving weather-related equipment problems.
The inspectors also reviewed
: [[BVPS]] [[design features and]]
FENOC's implementation of
procedures to handle issues that could impact offsite and alternating current (AC) power
systems. The inspectors reviewed
: [[FEN]] [[]]
OC's procedures and programs which discussed
the operation and availability/reliability of offsite and alternate AC power systems during adverse weather. The inspectors verified that communication protocols between the
transmission system operator and
: [[FEN]] [[]]
OC existed, and the appropriate information
would be conveyed when potential grid stress and disturbances existed. The inspectors
also verified that
: [[FEN]] [[]]
OC's procedures contained actions to monitor and maintain the
availability/reliability of offsite and onsite power systems prior to and during adverse weather conditions.
Enclosure b. Findings  No findings of significance were identified.
1R04 Equipment Alignment (71111.04) 
.1 Partial System Walkdowns (71111.04Q)
a. Inspection Scope (4 samples)  The inspectors performed four partial equipment alignment inspections during conditions
of increased safety significance, including when redundant equipment was unavailable
during maintenance or adverse conditions. The partial alignment inspections were also
completed after equipment was recently returned to service after significant
maintenance. The inspectors performed partial walkdowns of the following systems,
including associated electrical distribution components and control room panels, to verify
the equipment was aligned to perform its intended safety functions:  * Unit 1, on April 14, emergency diesel generator No. 1 during the performance of
: [[1OST]] [[-36.2, "Diesel Generator No. 2 Monthly Test;" * Unit 1, on April 16, train 'A' high head safety injection during the performance of 1]]
OST-7.19D, "Safety Injection Relay Test (Slave Relay K610)-Train B;" * Unit 1, on April 21, train 'B' residual heat removal system while 'A' electrical train was cleared for maintenance; and * Unit 1, on April 29, containment penetrations during the core reload.
b. Findings  No findings of significance were identified. 
.2 Complete System Walkdown (71111.04S)
a. Inspection Scope (2 samples)  The inspectors performed complete system walkdowns of the following systems to verify
that the critical portions, such as valve positions, switches, and breakers, were correctly
aligned in accordance with procedures, and to identify any discrepancies that may have
had an effect on operability.


The inspectors also reviewed outstanding maintenance work orders to verify that the
====a. Inspection Scope====
deficiencies did not significantly affect the system function. In addition, the inspectors
(1 sample)
discussed system health with the system engineer and reviewed the condition report
The purpose of this inspection was to assess the effectiveness of the licensee's in-service inspection (ISI) program for monitoring degradation of the reactor coolant system boundary, risk significant piping system boundaries, and the containment boundary for Unit 1. The inspector assessed the inservice inspection activities using the criteria specified in the American Society of Mechanical Engineers (ASME) Boiler and Pressure Vessel Code, Section XI and applicable NRC Regulatory Requirements. The inspector selected a sample of nondestructive examination (NDE) activities from the Unit 1 in-service inspection plan for the 1R19 outage for observation, documentation and record review, and evaluation for compliance with the requirements of the BVPS Unit 1 Risk-Informed Inservice Inspection Program and ASME Section XI. A sample of activities associated with the repair/replacement of safety related pressure boundary components was also reviewed. The sample selection was based on the inspection procedure objectives, risk significance, availability, and specifically on components and systems where degradation would result in a significant challenge to the integrity of pressure boundary components. The inspector also conducted a review of TI 2515/172, Reactor Coolant System Dissimilar Metal Butt Welds for Beaver Valley Power Station Unit 1.
database to verify that equipment alignment problems were being identified and
appropriately resolved. Documents reviewed during the inspection are listed in the
Attachment.  * On June 4, alignment and condition of the Unit 2 'C' service water pump and 'A' service water train while the 'D' main intake bay (affecting the 'A' service water
pump) was out of service for planned cleaning; and
Enclosure * On June 6, alignment of 'A' and 'B' motor-driven auxiliary and dedicated feedwater pumps while the turbine-driven feedwater pump was out of service for
planned maintenance.
b. Findings  No findings of significance were identified.
1R05 Fire Protection (71111.05) 
.1 Quarterly Sample Review (71111.05Q)
a. Inspection Scope (7 samples)  The inspectors reviewed the conditions of the fire areas listed below, to verify compliance
with criteria delineated in Administrative Procedure 1/2-ADM-1900, "Fire Protection,"
Rev. 19. This review included
: [[FEN]] [[]]
OC's control of transient combustibles and ignition
sources, material condition of fire protection equipment including fire detection systems,
water-based fire suppression systems, gaseous fire suppression systems, manual
firefighting equipment and capability, passive fire protection features, and the adequacy of compensatory measures for any fire protection impairments. Documents reviewed are
listed in the Attachment:  * Unit 2,
: [[TR]] [[-]]
: [[MT]] [[-2 Main Transformer (Fire Area]]
: [[TR]] [[-1); * Unit 2,]]
: [[TR]] [[-2C Unit Station Service Transformer (Fire Area]]
: [[TR]] [[-2); * Unit 2,]]
: [[TR]] [[-2D Unit Station Service Transformer (Fire Area]]
: [[TR]] [[-3); * Unit 1,]]
: [[AE]] [[Switchgear Room, Battery Rooms 1& 3 (Fire Area]]
: [[ES]] [[-1); * Unit 1,]]
: [[DF]] [[Switchgear Room, Battery Rooms 2& 4 (Fire Area]]
: [[ES]] [[-2); * Unit 1, Reactor Containment (Fire Area]]
RC-1); and * Unit 1, Rod Control Motor Generator Room (Fire Area MG-1)
b. Findings  No findings of significance were identified. 
.2 Annual Fire Drill Observation (71111.05A)
a. Inspection Scope (1 sample) The inspectors observed personnel performance during response to an indicated fire in
the Emergency Response Facility sub-station (also see Section 40A3.1) by the fire brigade on June 18. The inspection evaluated the station's demonstration of readiness
in fire fighting response. The inspectors observed the fire brigade members using
protective clothing, turnout gear, and self-contained breathing apparatus and entering the
fire area in a controlled manner. The inspectors also observed the fire fighting
equipment brought to the fire scene to evaluate whether sufficient equipment was
available to effectively control and extinguish the simulated fire. The inspectors
evaluated whether the permanent plant fire hose lines were capable of reaching the fire
area and whether hose usage was adequate. The inspectors observed the fire fighting
directions and communications between fire brigade members. The inspectors verified
Enclosure that the pre-fire plan was used and observed the post-event critique to evaluate fact-finding, lessons-learned and whether any immediate deficiencies needed addressed.
b. Findings  No findings of significance were identified.
1R06 Flood Protection Measures (71111.06)
a. Inspection Scope (1 sample - underground cables)  The inspectors reviewed a sample of internal flood protection measures regarding cables
located in underground manholes. The inspectors selected a
: [[FEN]] [[]]
OC inspection of
manholes 8A and 8B that contain Unit 1 and Unit 2 safety-related power and control
cables near the main intake structure. These cable manholes are underground and also
the focus of a focus problem identification and resolution review (see section 4OA2.3).
This review was conducted to evaluate
: [[FEN]] [[]]
OC's protection of the enclosed safety-
related systems from internal flooding condition. The inspectors entered the confined
area with
: [[FEN]] [[]]
OC personnel, inspected the manhole, and monitored licensee
maintenance activities. The inspectors also reviewed the
: [[UFS]] [[]]
AR, related internal
flooding evaluations, and other related documents. The inspectors examined the as-
found equipment and conditions to ensure that they remained consistent with those
indicated in the design basis documentation, flooding mitigation documents, and risk
analysis assumptions. Documents reviewed during the inspection are listed in the
Attachment.
b. Findings  One finding of significance was identified and documented in section 4OA2.3.
1R08 Unit 1 Inservice Inspection (IP 71111.08)
a. Inspection Scope (1 sample)  The purpose of this inspection was to assess the effectiveness of the licensee's in-
service inspection (ISI) program for monitoring degradation of the reactor coolant system
boundary, risk significant piping system boundaries, and the containment boundary for
Unit 1. The inspector assessed the inservice inspection activities using the criteria
specified in the American Society of Mechanical Engineers (ASME) Boiler and Pressure
Vessel Code, Section
: [[XI]] [[and applicable]]
NRC Regulatory Requirements. The inspector
selected a sample of nondestructive examination (NDE) activities from the Unit 1 in-
service inspection plan for the 1R19 outage for observation, documentation and record
review, and evaluation for compliance with the requirements of the
: [[BV]] [[]]
PS Unit 1 Risk-
Informed Inservice Inspection Program and
: [[ASME]] [[Section]]
XI. A sample of activities
associated with the repair/replacement of safety related pressure boundary components
was also reviewed. The sample selection was based on the inspection procedure
objectives, risk significance, availability, and specifically on components and systems where degradation would result in a significant challenge to the integrity of pressure
boundary components. The inspector also conducted a review of TI 2515/172, Reactor
Coolant System Dissimilar Metal Butt Welds for Beaver Valley Power Station Unit 1.


Enclosure The inspector reviewed in-process
The inspector reviewed in-process NDE, examination data records, deficiency reports and interviewed NDE personnel to evaluate t he technician skills and performance, test equipment capabilities, and examination techniques and to verify that the activities, including calibration, set-up, examination techniques, data analysis, and that indications and defects were evaluated and dispositioned in accordance with ASME Boiler and Pressure Vessel Code, 2001 Edition to 2003 Addenda Section XI, relevant ASME Code Cases, selected relief requests, BVPS Unit 1 Risk-Informed Inservice Inspection Program, the Materials Reliability Program (MRP)recommendations, and compliance with 10CFR 50.55a.
: [[NDE]] [[, examination data records, deficiency reports and interviewed]]
NDE personnel to evaluate the technician skills and performance, test equipment capabilities, and examination techniques and to verify that the activities, including calibration, set-up, examination techniques, data analysis, and that indications
and defects were evaluated and dispositioned in accordance with
: [[AS]] [[]]
ME Boiler and
Pressure Vessel Code, 2001 Edition to 2003 Addenda Section
: [[XI]] [[, relevant]]
ASME Code
Cases, selected relief requests,
: [[BV]] [[]]
PS Unit 1 Risk-Informed Inservice Inspection
Program, the Materials Reliability Program (MRP) recommendations, and compliance with 10CFR 50.55a.  


The inspector also verified that observed indications and deficient conditions were being
The inspector also verified that observed indications and deficient conditions were being adequately entered and dispositioned in the BVPS corrective action program.
adequately entered and dispositioned in the
: [[BV]] [[]]
PS corrective action program.  


Non-Destructive Examination (NDE) and Welding Activities
Non-Destructive Examination (NDE) and Welding Activities
The following dye penetrant testing (PT), ultrasonic testing (UT), magnetic particle testing
(MT), and visual testing (VT) activities performed during 1R19 outage were reviewed by
the inspector.


The inspector observed and reviewed a sample of NDE examinations and
The following dye penetrant testing (PT), ultrasonic testing (UT), magnetic particle testing (MT), and visual testing (VT) activities performed during 1R19 outage were reviewed by the inspector.
documentation records of manual
 
: [[UT]] [[examination of reactor coolant system (]]
The inspector observed and reviewed a sample of NDE examinations and documentation records of manual UT examination of reactor coolant system (RCS) 'A' loop cold and hot leg nozzle-to-safe-end dissimilar metal (DM) welds RC-E-1A-N11 and RC-E-1A-N12 and RCS 'C' loop cold leg pipe girth weld DLW-LOOP3-7-S-02 performed as follow-up UT examination for a flaw indication initially identified in March 1996. The inspector reviewed visual bare metal inspections (BMI) records and photos of the Unit 1 reactor pressure vessel lower head penetration nozzles. The resident inspection staff directly observed VT boric acid walk-down inspections inside the Unit 1 containment.
RCS) 'A'
loop cold and hot leg nozzle-to-safe-end dissimilar metal (DM) welds
: [[RC]] [[-E-1A-N11 and]]
: [[RC]] [[-E-1A-N12 and]]
: [[RCS]] [['C' loop cold leg pipe girth weld]]
: [[DLW]] [[-]]
LOOP3-7-S-02 performed
as follow-up UT examination for a flaw indication initially identified in March 1996. The
inspector reviewed visual bare metal inspections (BMI) records and photos of the Unit 1
reactor pressure vessel lower head penetration nozzles. The resident inspection staff
directly observed VT boric acid walk-down inspections inside the Unit 1 containment.
The inspector also performed a document review of UT thickness examination data
records of the Unit 1 containment liner, which was an examination in the area around a
through-wall hole that was identified during 1R19 outage and magnetic particle and UT
examinations of the liner replacement repairs, UT thickness examination data records of
the Unit 1 containment liner area #3, and PT examination data record of residual heat
removal (RHR) welded attachment RH-1-1-A-02.  


Qualified
The inspector also performed a document review of UT thickness examination data records of the Unit 1 containment liner, which was an examination in the area around a through-wall hole that was identified during 1R19 outage and magnetic particle and UT examinations of the liner replacement repairs, UT thickness examination data records of the Unit 1 containment liner area #3, and PT examination data record of residual heat removal (RHR) welded attachment RH-1-1-A-02.
: [[FEN]] [[]]
 
OC inspectors visually examined the condition of accessible portions of the
Qualified FENOC inspectors visually examined the condition of accessible portions of the containment, including the inside surface of the containment liner for corrosion, mechanical damage and other degradation mechanisms during the 1R19 outage. As a result of an observed blister in the protective paint coating and protruding rust on the inside surface of the containment liner at the 738' elevation, a work order was written to clean the area to allow further evaluation. The cleaning activity uncovered a through-wall corrosion rectangular hole approximately 1" (horizontal) x 3/8" (vertical) in the containment liner which was documented in CR 09-57589 and 09-57762 and reported to the NRC per 10CFR50.72 on April 23, 2009. Manual UT thickness examinations of the containment liner of the affected area were taken as part of ASME Section XI, Subsection IWE to determine the extent of the liner corrosion. The inspectors observed various aspects of the containment liner NDE inspections, liner plate replacement, repair welding, and testing activities during the 1R19 outage. A more detailed inspection and assessment of the containment liner through-wall corrosion hole is documented in inspection report 05000334/2009006.
containment, including the inside surface of the containment liner for corrosion,
 
mechanical damage and other degradation mechanisms during the 1R19 outage. As a
The inspector examined disposition for continued operation, without repair or rework, of non-conforming condition indications identified during 1R19 outage ISI activities. The inspector reviewed a liquid penetrant (PT) examination report PT-09-1003 and evaluation report EV-09-1002 of welded attachment RH-1-1-A-02, located on an RHR system elbow for spring can hanger SH-40, which identified a liner indication at the attachment/elbow interface area that wa s determined acceptable after light filling of the surface indication.
result of an observed blister in the protective paint coating and protruding rust on the
inside surface of the containment liner at the 738' elevation, a work order was written to
clean the area to allow further evaluation. The cleaning activity uncovered a through-wall
corrosion rectangular hole approximately 1" (horizontal) x 3/8" (vertical) in the
containment liner which was documented in CR 09-57589 and 09-57762 and reported to
the
: [[NRC]] [[per 10]]
CFR50.72 on April 23, 2009. Manual UT thickness examinations of the
containment liner of the affected area were taken as part of
: [[ASME]] [[Section]]
XI,
Subsection IWE to determine the extent of the liner corrosion. The inspectors observed
various aspects of the containment liner NDE inspections, liner plate replacement, repair
welding, and testing activities during the 1R19 outage. A more detailed inspection and
assessment of the containment liner through-wall corrosion hole is documented in
inspection report 05000334/2009006.  


Enclosure The inspector examined disposition for continued operation, without repair or rework, of non-conforming condition indications identified during 1R19 outage ISI activities. The
inspector reviewed a liquid penetrant (PT) examination report PT-09-1003 and evaluation
report
: [[EV]] [[-09-1002 of welded attachment]]
RH-1-1-A-02, located on an RHR system elbow
for spring can hanger SH-40, which identified a liner indication at the attachment/elbow
interface area that was determined acceptable after light filling of the surface indication.
Repair/Replacement Consisting of Welding
Repair/Replacement Consisting of Welding
Ultrasonic (UT) examinations performed on base material per the Materials Reliability
 
Program (MRP) MRP-146 recommendations identified two circumferential indications
Ultrasonic (UT) examinations performed on base material per the Materials Reliability Program (MRP) MRP-146 recommendations identified two circumferential indications approximately 3/8 inches in length in the stainless steel base material adjacent to a socket weld on the horizontal portion of BV-1RC-41, a 2-inch drain line connected to the "A" reactor coolant system (RCS) Hot Leg. The deficient condition was documented in CR 09-58004 and work order 200367565 was initiated to replace the affected piping segment of the 2-inch drain line. To verify suitability of materials, welding activities performed, applicable NDE performed, and ISI implementing procedures were in accordance with the ASME code requirements the inspector reviewed the work scope, activity sequence, weld filler metal selection, welding pr ocedure, non-destructive examination tests, acceptance criteria and post work testing.
approximately 3/8 inches in length in the stainless steel base material adjacent to a
socket weld on the horizontal portion of
: [[BV]] [[-1]]
RC-41, a 2-inch drain line connected to the  
"A" reactor coolant system (RCS) Hot Leg. The deficient condition was documented in
CR 09-58004 and work order 200367565 was initiated to replace the affected piping
segment of the 2-inch drain line. To verify suitability of materials, welding activities
performed, applicable
: [[NDE]] [[performed, and]]
ISI implementing procedures were in
accordance with the
: [[AS]] [[]]
ME code requirements the inspector reviewed the work scope,
activity sequence, weld filler metal selection, welding procedure, non-destructive examination tests, acceptance criteria and post work testing.  


Reactor Pressure Vessel Lower Head Penetration Nozzle Inspection
Reactor Pressure Vessel Lower Head Penetration Nozzle Inspection
The inspector verified the inspection results of the visual BMI of the Unit 1 reactor
 
pressure vessel lower head penetration nozzles that was conducted by
The inspector verified the inspection results of the visual BMI of the Unit 1 reactor pressure vessel lower head penetration nozzles that was conducted by VT-qualified FENOC personnel during 1R19 by reviewing visual inspection documentation record results and photos of the BMI inspection. No boric acid leakage was observed around the annulus area on the 43 penetrations inspected.
: [[VT]] [[-qualified]]
: [[FEN]] [[]]
OC personnel during 1R19 by reviewing visual inspection documentation record
results and photos of the BMI inspection. No boric acid leakage was observed around
the annulus area on the 43 penetrations inspected.  


Pressurized Water Reactor Vessel Upper Head Penetration Inspection
Pressurized Water Reactor Vessel Upper Head Penetration Inspection
No inspections were performed of the
 
: [[BV]] [[]]
No inspections were performed of the BVPS Unit 1 reactor vessel upper head during  
PS Unit 1 reactor vessel upper head during
 
1R19 outage because the Unit 1 reactor vessel head was replaced in 2006 during 1R17
{{a|1R19}}
outage. The inspector reviewed applicable
==1R19 outage because the Unit 1 reactor vessel head was replaced in 2006 during 1R17==
: [[NRC]] [[Regulatory Requirements and]]
 
ASME
outage. The inspector reviewed applicable NRC Regulatory Requirements and ASME Code, Section XI, to verify that no examinations were required of the Unit 1 reactor vessel upper head.
Code, Section XI, to verify that no examinations were required of the Unit 1 reactor
vessel upper head.  


Boric Acid Corrosion Control (BACC) Inspection Activities
Boric Acid Corrosion Control (BACC) Inspection Activities
The inspector discussed the boric acid control program controlled by
: [[BV]] [[]]
: [[PS]] [[procedure]]
: [[NOP]] [[-]]
ER-2001, Boric Acid Corrosion Control Program with the boric acid corrosion
control program owner and sampled photographic inspections of boric acid found on
safety significant piping and components inside Unit 1containment during Mode 3 walk
downs conducted by
: [[FEN]] [[]]
OC personnel in April 2009. The walk down was directly
observed by the resident inspection staff, to verify that the visual inspections were
performed in accordance with the procedure and checklists which emphasized the areas
and locations where boric acid leaks could cause degradation of safety significant
components and that deficient conditions were identified and documented.
Approximately 138 locations were identified with boric acid during 1R19 walk down
inspections. 


Enclosure A sample of engineering evaluations/corrective actions associated with these boric acid deficiencies and a sample of these items on the Unit 1 mode hold list were reviewed by
The inspector discussed the boric acid control program controlled by BVPS procedure NOP-ER-2001, Boric Acid Corrosion Control Program with the boric acid corrosion control program owner and sampled photographic inspections of boric acid found on safety significant piping and components inside Unit 1containment during Mode 3 walk downs conducted by FENOC personnel in April 2009. The walk down was directly observed by the resident inspection staff, to verify that the visual inspections were performed in accordance with the procedure and checklists which emphasized the areas and locations where boric acid leaks could cause degradation of safety significant components and that deficient conditions were identified and documented.
the inspector. The inspector confirmed that condition reports were assigned corrective
 
actions consistent with the requirements of the
Approximately 138 locations were identified with boric acid during 1R19 walk down inspections.
: [[ASME]] [[Code and 10]]
 
CFR 50, Appendix B,
A sample of engineering evaluations/corrective actions associated with these boric acid deficiencies and a sample of these items on the Unit 1 mode hold list were reviewed by the inspector. The inspector confirmed that condition reports were assigned corrective actions consistent with the requirements of the ASME Code and 10 CFR 50, Appendix B, Criterion XVI. The inspector reviewed various condition reports and work orders to resolve the identified deficient boric acid conditions.
Criterion XVI. The inspector reviewed various condition reports and work orders to
 
resolve the identified deficient boric acid conditions.  
Steam Generator (SG) Tube Inspections The inspectors reviewed the BVPS Unit 1 1R18 steam generator degradation assessment SG-CDME-07-24. No inspections were performed of the BVPS Unit 1 steam generator tubes during 1R19 outage because the Unit 1 steam generators were replaced in 2006 during 1R17 outage. The inspector reviewed applicable NRC Regulatory Requirements and the ASME Code Section XI to verify that no examinations were required during 1R19.
 
Problem Identification and Resolution The inspector reviewed a sample of condition reports related to ISI, MRP-139, and MRP-146 program activities to assess FENOC's effectiveness in problem identification and resolution and determined that deficiencies are being appropriately identified, and entered into and resolved by the corrective action program.
{{a|1R11}}
==1R11 Licensed Operator Requalification Program==
{{IP sample|IP=IP 71111.11Q}}


Steam Generator (SG) Tube Inspections  The inspectors reviewed the
====a. Inspection Scope====
: [[BV]] [[]]
(1 sample)
PS Unit 1 1R18 steam generator degradation
The inspectors observed Unit 2 licensed operator simulator training on June 23. The inspectors evaluated licensed operator performance regarding command and control, implementation of normal, annunciator response, abnormal, and emergency operating procedures, communications, technical specification review and compliance, and emergency plan implementation. The inspectors evaluated the licensee staff training personnel to verify that deficiencies in operator performance were identified, and that conditions adverse to quality were entered into the licensee's corrective action program for resolution. The inspectors reviewed simulator physical fidelity to assure the simulator appropriately modeled the plant control room. The inspectors verified that the training evaluators adequately addressed that the applicable training objectives had been achieved.
assessment
 
: [[SG]] [[-]]
====b. Findings====
: [[CDME]] [[-07-24. No inspections were performed of the]]
No findings of significance were identified.
: [[BV]] [[]]
{{a|1R12}}
PS Unit 1
==1R12 Maintenance Rule Implementation==
steam generator tubes during 1R19 outage because the Unit 1 steam generators were
{{IP sample|IP=IP 71111.12Q}}
replaced in 2006 during 1R17 outage. The inspector reviewed applicable
 
: [[NRC]] [[Regulatory Requirements and the]]
====a. Inspection Scope====
: [[ASME]] [[Code Section]]
(2 samples)
XI to verify that no examinations
The inspectors evaluated Maintenance Rule (MR) implementation for the issues listed below. The inspectors evaluated specific attributes, such as MR scoping, characterization of failed structures, systems, and components (SSCs), MR risk characterization of SSCs, SSC performance criteria and goals, and appropriateness of corrective actions. The inspectors verified that the issues were addressed as required by 10 CFR 50.65 and the licensee's program for MR implementation. For the selected SSCs, the inspectors evaluated whether performance was properly dispositioned for MR category (a)(1) and (a)(2) performance monitoring. MR System Basis Documents were also reviewed, as appropriate.
were required during 1R19.  
* Unit 1, Solid State Protection System does not achieve MR a(1) goals, as documented in CR 09-59359; and
* Unit 1, 1CCP-P-1A, head ratio greater than acceptance criteria as documented in CR 09-60127.
 
====b. Findings====
No findings of significance were identified.
{{a|1R13}}
==1R13 Maintenance Risk Assessment and Emergent Work Control==
{{IP sample|IP=IP 71111.13}}
 
====a. Inspection Scope====
(5 samples)
The inspectors reviewed the scheduling and control of five activities, and evaluated their effect on overall plant risk. This review was conducted to ensure compliance with applicable criteria contained in 10 CFR 50.65(a)(4). Documents reviewed during the inspection are listed in the Attachment.
* On April 20, Unit 1 refueling outage defense-in-depth report re-assessment for changes in calculated time-to-boil values, as document in CR 09-57463;
* On April 21, Unit 1 yellow shutdown risk during EDG 1-1 autoload test;
* On May 3, Unit 1 change in shutdown risk profile for repairs to "B" Residual Heat Removal Pump (1DRH-P-1A) (CR 09-58513);
* Week of June 1, Unit 1 and Unit 2, review of station risk during planned 'D' main intake bay cleaning; and
* During June 15-21, Unit 1 and Unit 2, review of changed and emergent work coordination for that planned week's activities, including a review of station processes and procedures for risk determination.
 
====b. Findings====
No findings of significance were identified.
{{a|1R15}}
==1R15 Operability Evaluations==
{{IP sample|IP=IP 71111.15}}
 
====a. Inspection Scope====
(6 samples)
The inspectors evaluated the technical adequacy of se lected immediate operability determinations (I OD), prompt operability determinations (POD), or functionality assessments (FA), to verify that determinations of Technical Specifications (TS)operability were justified, as appropriate. In additi on, the inspectors verified that TS limiting conditions for operation (LCO) requirements and UFSAR design basis requirements were properly addressed. In addition, the inspectors reviewed compensatory measures implemented to ensure the measures worked and were adequately controlled. Documents reviewed are listed in the Attachment.
* April 12 -14, Unit 1 turbine-driven auxiliary feedwater pump (FW-P-2) steam isolation valve (MOV-1MS-105) failed to open electrically as documented in CR 09-57106;
* On April 15, Unit 1 & 2, licensee's review and assessment of NRC Regulatory Issue Summary 2009-02 documented in CR 09-57275;
* On April 21, Unit 1 primary component cooler inlet temperature indicator failure to containment penetration cooling coils documented in CR 09-57667;
* On April 23, Unit 1 containment liner plate degradation documented in CRs 09-57589, 09-57762;
* On May 6, Unit 1 emergency diesel generator 1-2 original governor re-installation due to issues documented in CR 09-58435; and
* On June 16, Unit 2 licensee's functional assessment regarding fire protection safe shutdown report analysis of station air documented in CRs 09-60058, 09-60162, 06-6932.
 
====b. Findings====
No findings of significance were identified.
{{a|1R18}}
==1R18 Plant Modifications==
{{IP sample|IP=IP 71111.18}}
===.1 Temporary Plant Modifications===
 
====a. Inspection Scope====
(2 samples)
The inspectors reviewed the following temporary modifications (TMOD) based on risk significance. The TMOD and associated 10 CFR 50.59 screening were reviewed against the system design basis documentation, including the UFSAR and the TS. The inspectors verified the TMODs were implemented in accordance with Administrative (ADM) Procedure, 1/2-ADM-2028, "Temporary Modifications," Rev. 9. Documents reviewed are listed in the Attachment.
* TMOD ECP 09-0174 to provide an alternate discharge path for Unit 1 river water from the outlet of 'A' emergency diesel generator heat exchanger (1EE-E-1A) to the normal discharge catch basin; and
* TMOD ECP 09-01453 to provide additional mitigating configuration and control of plant operations during solid plant operation while shutdown.
 
====b. Findings====
No findings of significance were identified.
 
===.2 Permanent Plant Modifications===
 
====a. Inspection Scope====
(1 sample)
The inspectors evaluated the design basis impact of the modification to the Unit 1 reactor trip breaker circuit under ECP 08-0134-002. The inspectors reviewed the adequacy of the associated 10 CFR 50.59 screening, verified that attributes and parameters within the design documentation were consistent with required licensing and design bases, as well as credited codes and standards, and observed portions of the modification to verify that changes described in the package were appropriately implemented. The inspectors also verified the post-modification testing was satisfactorily accomplished to ensure the system and components operated consistent with their intended safety function.


Problem Identification and Resolution  The inspector reviewed a sample of condition reports related to
: [[ISI]] [[,]]
MRP-139, and MRP-
146 program activities to assess
: [[FEN]] [[]]
OC's effectiveness in problem identification and
resolution and determined that deficiencies are being appropriately identified, and
entered into and resolved by the corrective action program.
1R11 Licensed Operator Requalification Program (71111.11Q)
a. Inspection Scope  (1 sample)  The inspectors observed Unit 2 licensed operator simulator training on June 23. The
inspectors evaluated licensed operator performance regarding command and control,
implementation of normal, annunciator response, abnormal, and emergency operating
procedures, communications, technical specification review and compliance, and
emergency plan implementation. The inspectors evaluated the licensee staff training
personnel to verify that deficiencies in operator performance were identified, and that
conditions adverse to quality were entered into the licensee's corrective action program
for resolution. The inspectors reviewed simulator physical fidelity to assure the simulator
appropriately modeled the plant control room. The inspectors verified that the training
evaluators adequately addressed that the applicable training objectives had been
achieved.
b. Findings  No findings of significance were identified.
1R12 Maintenance Rule Implementation (71111.12Q)
a. Inspection Scope (2 samples)  The inspectors evaluated Maintenance Rule (MR) implementation for the issues listed
below. The inspectors evaluated specific attributes, such as MR scoping,
characterization of failed structures, systems, and components (SSCs), MR risk
characterization of
: [[SSC]] [[s,]]
SSC performance criteria and goals, and appropriateness of
Enclosure corrective actions. The inspectors verified that the issues were addressed as required by
: [[10 CFR]] [[50.65 and the licensee's program for]]
: [[MR]] [[implementation. For the selected]]
: [[SSC]] [[s, the inspectors evaluated whether performance was properly dispositioned for]]
MR
category (a)(1) and (a)(2) performance monitoring. MR System Basis Documents were
also reviewed, as appropriate.
* Unit 1, Solid State Protection System does not achieve
: [[MR]] [[a(1) goals, as documented in]]
: [[CR]] [[09-59359; and  * Unit 1,]]
: [[1CCP]] [[-P-1A, head ratio greater than acceptance criteria as documented in]]
CR 09-60127.
b. Findings  No findings of significance were identified.
1R13  Maintenance Risk Assessment and Emergent Work Control (71111.13)
a. Inspection Scope (5 samples)  The inspectors reviewed the scheduling and control of five activities, and evaluated
their effect on overall plant risk. This review was conducted to ensure compliance with
applicable criteria contained in 10 CFR 50.65(a)(4). Documents reviewed during the
inspection are listed in the Attachment.  * On April 20, Unit 1 refueling outage defense-in-depth report re-assessment for changes in calculated time-to-boil values, as document in
: [[CR]] [[09-57463; * On April 21, Unit 1 yellow shutdown risk during]]
EDG 1-1 autoload test; * On May 3, Unit 1 change in shutdown risk profile for repairs to "B" Residual Heat Removal Pump (1DRH-P-1A) (CR 09-58513); * Week of June 1, Unit 1 and Unit 2, review of station risk during planned 'D' main intake bay cleaning; and * During June 15-21, Unit 1 and Unit 2, review of changed and emergent work coordination for that planned week's activities, including a review of station
processes and procedures for risk determination. b. Findings  No findings of significance were identified.
1R15 Operability Evaluations (71111.15)
a. Inspection Scope (6 samples)  The inspectors evaluated the technical adequacy of selected immediate operability determinations (IOD), prompt operability determinations (POD), or functionality assessments (FA), to verify that determinations of Technical Specifications (TS)
operability were justified, as appropriate. In addition, the inspectors verified that
: [[TS]] [[limiting conditions for operation (]]
: [[LCO]] [[) requirements and]]
: [[UFS]] [[]]
AR design basis
requirements were properly addressed. In addition, the inspectors reviewed
Enclosure compensatory measures implemented to ensure the measures worked and were adequately controlled. Documents reviewed are listed in the Attachment.    * April 12 -14, Unit 1 turbine-driven auxiliary feedwater pump (FW-P-2) steam isolation valve (MOV-1MS-105) failed to open electrically as documented in
: [[CR]] [[09-57106; * On April 15, Unit 1 & 2, licensee's review and assessment of]]
: [[NRC]] [[Regulatory Issue Summary 2009-02 documented in]]
: [[CR]] [[09-57275; * On April 21, Unit 1 primary component cooler inlet temperature indicator failure to containment penetration cooling coils documented in]]
: [[CR]] [[09-57667; * On April 23, Unit 1 containment liner plate degradation documented in]]
: [[CR]] [[s 09-57589, 09-57762; * On May 6, Unit 1 emergency diesel generator 1-2 original governor re-installation due to issues documented in]]
: [[CR]] [[09-58435; and * On June 16, Unit 2 licensee's functional assessment regarding fire protection safe shutdown report analysis of station air documented in]]
CRs 09-60058, 09-
60162, 06-6932.
b. Findings  No findings of significance were identified.
1R18  Plant Modifications (71111.18)  .1 Temporary Plant Modifications
a. Inspection Scope (2 samples)  The inspectors reviewed the following temporary modifications (TMOD) based on risk
significance. The
: [[TMOD]] [[and associated 10]]
CFR 50.59 screening were reviewed against
the system design basis documentation, including the
: [[UFSAR]] [[and the]]
TS. The
inspectors verified the
: [[TM]] [[]]
ODs were implemented in accordance with Administrative
(ADM) Procedure, 1/2-ADM-2028, "Temporary Modifications," Rev. 9. Documents
reviewed are listed in the Attachment.  *
: [[TMOD]] [[]]
ECP 09-0174 to provide an alternate discharge path for Unit 1 river water from the outlet of 'A' emergency diesel generator heat exchanger (1EE-E-1A) to
the normal discharge catch basin; and *
: [[TMOD]] [[]]
ECP 09-01453 to provide additional mitigating configuration and control of plant operations during solid plant operation while shutdown.
b. Findings  No findings of significance were identified. 
.2 Permanent Plant Modifications
a. Inspection Scope (1 sample)
Enclosure The inspectors evaluated the design basis impact of the modification to the Unit 1 reactor trip breaker circuit under ECP 08-0134-002. The inspectors reviewed the adequacy of
the associated 10 CFR 50.59 screening, verified that attributes and parameters within
the design documentation were consistent with required licensing and design bases, as
well as credited codes and standards, and observed portions of the modification to verify
that changes described in the package were appropriately implemented. The inspectors
also verified the post-modification testing was satisfactorily accomplished to ensure the
system and components operated consistent with their intended safety function.
Documents reviewed are listed in the Attachment.
Documents reviewed are listed in the Attachment.
b. Findings  No findings of significance were identified.
1R19 Post-Maintenance Testing (71111.19)
a. Inspection Scope (7 samples)  The inspectors reviewed the following activities to determine whether the post-
maintenance tests (PMT) adequately demonstrated that the safety-related function of the
equipment was satisfied given the scope of the work, and that operability of the system was restored. In addition, the inspectors evaluated the applicable acceptance criteria to
verify consistency with the design and licensing bases, as well as TS requirements. The
inspectors witnessed the test or reviewed test data to verify results adequately
demonstrated restoration of affected safety functions. The inspectors also verified that
conditions adverse to quality were entered into the corrective action program for
resolution. Documents reviewed during the inspection are listed in the Attachment.  * On April 3,
: [[1OST]] [[-30.3, after planned maintenance on Unit 1 'B' train river water; * On April 14, Unit 1, new-fuel frame hoist motor (1]]
: [[FN]] [[-W-1-MOTOR) cable replacement; * On April 21, Unit 1, replacement and retest of]]
: [[VSR]] [[2 in No.1-1 emergency diesel output breaker (4]]
: [[KVS]] [[-1AE-1E9) control circuit; * On May 6, Unit 1, emergency diesel generator No. 1-2 (1EE-EG-2) governor replacement; * On May 8, Unit 1, final painting and baseline volumetric scan after containment plate liner repair; * On May 19, Unit 1, replacement of number 2 seal on 'A' reactor coolant pump; and * On May 30, Unit 1, replacement of]]
: [[1RW]] [[-57, 'A' river water pump (1]]
: [[WR]] [[-P-1A) discharge check valve. b. Findings  Introduction: A self-revealing Green]]
: [[NCV]] [[of 10]]
CFR Part 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings" was identified for failure to specify and perform
an adequate PMT after replacing a safety-related river water check-valve. Specifically,
train 'A' river water was declared operable after replacement of check valve 1RW-57 per
work order 200233562 without an adequate PMT.   


Enclosure Description: On May 25, 2009, the 'A' main intake bay was removed from service for planned bay cleaning. This rendered the 'A' safety-related river water pump (1WR-P-1A)
====b. Findings====
inoperable. The spare 'C' river water pump (1WR-P-1C) was aligned to service the 'A'
No findings of significance were identified.
river train. During the bay cleaning, the 'A' river water pump discharge check valve
{{a|1R19}}
(1RW-57) was replaced on May 28 by mechanical maintenance per work order
==1R19 Post-Maintenance Testing==
200233562. This work order did not specify PMT requirements. The work order was
{{IP sample|IP=IP 71111.19}}
signed complete and the 'A' intake bay was returned to service on May 28. On May 29
the 'A' river water train was re-aligned, placing the 1WR-P-1A pump in service and
operable at 12:25 p.m. At 2:40 p.m., it was identified that PMT was not performed for
replacement of 1RW-57. The shift manager immediately declared 'A' train river water
inoperable and aligned the WR-P-1C to serve the 'A' river water train.  


The inservice testing coordinator was contacted to identify post-maintenance testing
====a. Inspection Scope====
requirements.
(7 samples)
: [[ASME]] [[]]
The inspectors reviewed the following activities to determine whether the post-maintenance tests (PMT) adequately demonstrated that the safety-related function of the equipment was satisfied given the scope of the work, and that operability of the system was restored. In addition, the inspectors evaluated the applicable acceptance criteria to verify consistency with the design and licensing bases, as well as TS requirements. The inspectors witnessed the test or reviewed test data to verify results adequately demonstrated restoration of affected safety functions. The inspectors also verified that conditions adverse to quality were entered into the corrective action program for resolution. Documents reviewed during the inspection are listed in the Attachment.
: [[OM]] [[Code, Section]]
* On April 3, 1OST-30.3, after planned maintenance on Unit 1 'B' train river water;
: [[IS]] [[]]
* On April 14, Unit 1, new-fuel frame hoist motor (1FN-W-1-MOTOR) cable replacement;
TC-5221 requires a forward flow and reverse-
* On April 21, Unit 1, replacement and retest of VSR2 in No.1-1 emergency diesel output breaker (4KVS-1AE-1E9) control circuit;
closure verification for post-maintenance testing following a check valve replacement.
* On May 6, Unit 1, emergency diesel generator No. 1-2 (1EE-EG-2) governor replacement;
The PMT was accomplished satisfactorily on June 1.
* On May 8, Unit 1, final painting and baseline volumetric scan after containment plate liner repair;
* On May 19, Unit 1, replacement of number 2 seal on 'A' reactor coolant pump; and
* On May 30, Unit 1, replacement of 1RW-57, 'A' river water pump (1WR-P-1A) discharge check valve.


The licensee's post-maintenance process failed to specify an adequate PMT for the
====b. Findings====
check valve replacement. The work order lacked any operational PMT and was the
apparent cause of the performance deficiency. The licensee documented this issue in
CR 09-59866.  


Analysis: The failure to specify and perform a PMT after replacing a safety-related river water check-valve was a performance deficiency. The inspectors determined that the
=====Introduction:=====
performance deficiency was not similar to the examples for minor deficiencies contained
A self-revealing Green NCV of 10CFR Part 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings" was identified for failure to specify and perform an adequate PMT after replacing a safety-related river water check-valve. Specifically, train 'A' river water was declared operable after replacement of check valve 1RW-57 per work order 200233562 without an adequate PMT.
in IMC 0612, Appendix E, "Examples of Minor Issues". The finding was more than minor
in accordance with IMC 0612, Appendix B (Section 1-3), "Issue Screening," because the
failure to specify and perform a PMT is associated with the procedure quality
performance attribute of the mitigating systems cornerstone and affects the associated
cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences.  


In accordance with IMC 0609.04 (Table 4a), "Phase 1 - Initial Screening and
=====Description:=====
Characterization of Findings," the finding was determined to be of very low safety
On May 25, 2009, the 'A' main intake bay was removed from service for planned bay cleaning. This rendered the 'A' safety-related river water pump (1WR-P-1A)inoperable. The spare 'C' river water pump (1WR-P-1C) was aligned to service the 'A' river train. During the bay cleaning, the 'A' river water pump discharge check valve (1RW-57) was replaced on May 28 by mechanical maintenance per work order 200233562. This work order did not specify PMT requirements. The work order was signed complete and the 'A' intake bay was returned to service on May 28. On May 29 the 'A' river water train was re-aligned, placing the 1WR-P-1A pump in service and operable at 12:25 p.m. At 2:40 p.m., it was identified that PMT was not performed for replacement of 1RW-57. The shift manager immediately declared 'A' train river water inoperable and aligned the WR-P-1C to serve the 'A' river water train.
significance (Green) because the finding was not a design or qualification deficiency
which resulted in a loss of function.  


This finding has a crosscutting aspect in the area of human performance associated with
The inservice testing coordinator was contacted to identify post-maintenance testing requirements. ASME OM Code, Section ISTC-5221 requires a forward flow and reverse-closure verification for post-maintenance testing following a check valve replacement.
resources because the licensee did not have complete, accurate, and up-to-date
 
maintenance work procedures [H.2(c)].  
The PMT was accomplished satisfactorily on June 1.
 
The licensee's post-maintenance process failed to specify an adequate PMT for the check valve replacement. The work order lacked any operational PMT and was the apparent cause of the performance deficiency. The licensee documented this issue in CR 09-59866.
 
=====Analysis:=====
The failure to specify and perform a PMT after replacing a safety-related river water check-valve was a performance deficiency. The inspectors determined that the performance deficiency was not similar to the examples for minor deficiencies contained in IMC 0612, Appendix E, "Examples of Minor Issues". The finding was more than minor in accordance with IMC 0612, Appendix B (Section 1-3), "Issue Screening," because the failure to specify and perform a PMT is associated with the procedure quality performance attribute of the mitigating systems cornerstone and affects the associated
 
cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences.
 
In accordance with IMC 0609.04 (Table 4a), "Phase 1 - Initial Screening and Characterization of Findings," the finding was determined to be of very low safety significance (Green) because the finding was not a design or qualification deficiency which resulted in a loss of function.
 
This finding has a crosscutting aspect in the area of human performance associated with resources because the licensee did not have complete, accurate, and up-to-date maintenance work procedures [H.2(c)].  
 
=====Enforcement:=====
10 CFR 50, Appendix B, Criterion V, requires, in part, that procedures for performing maintenance that can affect the performance of safety-related equipment should be properly preplanned and performed in accordance with written procedures, documented instructions, or drawings appropriate to the circumstances. Contrary to this requirement, in May 2009, FENOC failed to specify and perform PMT after replacement of check value 1RW-57 prior to returning the system to operable status. Because this deficiency is considered to be of very low safety significance (Green), and was entered into the corrective action program (CR 09-59866), this violation is being treated as an NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy. (NCV 5000334/2009003-01, Inadequate Post-Maintenance Testing Specified for Safety-Related River Water Check Valve)
{{a|1R20}}
==1R20 Refueling and Outage Activities==
{{IP sample|IP=IP 71111.20}}
===.2 Unit 1 Refueling Outage (1R19)===
 
====a. Inspection Scope====
(1 sample)
The inspectors observed selected Unit 1 outage activities to determine whether shutdown safety functions (e.g. reactor decay heat removal, spent fool pool cooling, and containment integrity) were properly maintained as required by TS and plant procedures. The inspectors evaluated specific performance attributes including operator performance, communications, and instrumentation accuracy. The inspectors reviewed procedures and/or observed selected activities associated with the refueling outage. The inspectors verified activities were performed in accordance with procedures and verified required acceptance criteria were met. The inspectors also verified that conditions adverse to quality identified during performance of selected outage activities were identified by the licensee's corrective action program. Documents reviewed are listed in the Attachment. The inspectors also evaluated the following activities:
* Pre-outage shutdown safety review / defense-in-depth reports;
* Pre-outage temperature and power coastdown;
* Reactor plant shutdown and cooldown, including evaluation of cooldown rates;
* Solid plant operations;
* Configuration management, compliance with TS when taking equipment out of service;
* Implementation of clearance activities and confirmation that tags were hung properly;
* Status and configuration of electrical systems and switchyard activities;
* Monitoring of decay heat removal and spent fuel cooling;
* Fuel handling and activities that could affect reactivity;
* Final containment walkdown and closeout inspection;
* The digital video documenting the core reload and verification that fuel assembly placement was consistent with the reload map;
* Subsequent shutdown and cooldown to replace 'A' reactor coolant pump seals after initial startup for physics testing; and
* Final startup and power ascension to full power.
 
During the refueling outage FENOC identified a degradation of the containment liner during planned containment inspections. The review of this issue is documented in a separate report 05000334 / 2009006 (ADAMS ML091870328, on July 6, 2009). The inspectors also verified that refueling outage activities were in compliance with TS during


Enforcement: 10 CFR 50, Appendix B, Criterion V, requires, in part, that procedures for performing maintenance that can affect the performance of safety-related equipment
should be properly preplanned and performed in accordance with written procedures,
documented instructions, or drawings appropriate to the circumstances. Contrary to this
requirement, in May 2009,
: [[FENOC]] [[failed to specify and perform]]
PMT after replacement
of check value 1RW-57 prior to returning the system to operable status. Because this
deficiency is considered to be of very low safety significance (Green), and was entered
into the corrective action program (CR 09-59866), this violation is being treated as an
: [[NCV]] [[, consistent with Section]]
: [[VI.A.]] [[1 of the]]
: [[NRC]] [[Enforcement Policy. (]]
NCV
Enclosure 5000334/2009003-01, Inadequate Post-Maintenance Testing Specified for Safety-Related River Water Check Valve)
1R20 Refueling and Outage Activities (71111.20) 
.2 Unit 1 Refueling Outage (1R19)
a. Inspection Scope (1 sample)  The inspectors observed selected Unit 1 outage activities to determine whether
shutdown safety functions (e.g. reactor decay heat removal, spent fool pool cooling,
and containment integrity) were properly maintained as required by TS and plant
procedures. The inspectors evaluated specific performance attributes including operator
performance, communications, and instrumentation accuracy. The inspectors reviewed
procedures and/or observed selected activities associated with the refueling outage. The
inspectors verified activities were performed in accordance with procedures and verified
required acceptance criteria were met. The inspectors also verified that conditions
adverse to quality identified during performance of selected outage activities were
identified by the licensee's corrective action program. Documents reviewed are listed in
the Attachment. The inspectors also evaluated the following activities:  * Pre-outage shutdown safety review / defense-in-depth reports; * Pre-outage temperature and power coastdown; * Reactor plant shutdown and cooldown, including evaluation of cooldown rates; * Solid plant operations; * Configuration management, compliance with
: [[TS]] [[when taking equipment out of service; * Implementation of clearance activities and confirmation that tags were hung properly; * Status and configuration of electrical systems and switchyard activities; * Monitoring of decay heat removal and spent fuel cooling; * Fuel handling and activities that could affect reactivity; * Final containment walkdown and closeout inspection; * The digital video documenting the core reload and verification that fuel assembly placement was consistent with the reload map; * Subsequent shutdown and cooldown to replace 'A' reactor coolant pump seals after initial startup for physics testing; and * Final startup and power ascension to full power. During the refueling outage]]
FENOC identified a degradation of the containment liner
during planned containment inspections. The review of this issue is documented in a
separate report 05000334 / 2009006 (ADAMS ML091870328, on July 6, 2009). The
inspectors also verified that refueling outage activities were in compliance with TS during
the containment liner repair and retest. This issue was also reviewed for operability (section 1R15, 1R19) and event follow-up (section 4OA3.1)  
the containment liner repair and retest. This issue was also reviewed for operability (section 1R15, 1R19) and event follow-up (section 4OA3.1)  


The inspectors also observed selected management review activities associated with
The inspectors also observed selected management review activities associated with restart readiness of Unit 1, following completion of the 1R19 refueling activities. The restart readiness review meeting was accomplished as required by NOBP-OM-4010, "Restart Readiness for Plant Outages" Rev. 4, during the week of May 11. The purpose of the review, in part, was to assure that the plant's material condition, programs/processes, and personnel were ready for startup and safe, reliable operation after completion of outage activities.
restart readiness of Unit 1, following completion of the 1R19 refueling activities. The
 
restart readiness review meeting was accomplished as required by
====b. Findings====
: [[NOBP]] [[-]]
No findings of significance were identified.
OM-4010,  
{{a|1R22}}
"Restart Readiness for Plant Outages" Rev. 4, during the week of May 11. The purpose
==1R22 Surveillance Testing==
Enclosure of the review, in part, was to assure that the plant's material condition, programs/processes, and personnel were ready for startup and safe, reliable operation
{{IP sample|IP=IP 71111.22}}
after completion of outage activities.
 
b. Findings No findings of significance were identified.
====a. Inspection Scope====
1R22 Surveillance Testing (71111.22)
(8 samples: 1 isolation valve, 1 leak rate, 1 in-service testing and 5 routine.)
a. Inspection Scope (8 samples: 1 isolation valve, 1 leak rate, 1 in-service testing and 5 routine.) The inspectors witnessed the performance of or reviewed test data for the eight following
 
Operation Surveillance Test (OST) and Maintenance Surveillance (MSP) packages. The reviews verified that the equipment or systems were being tested as required by
The inspectors witnessed the performance of or reviewed test data for the eight following Operation Surveillance Test (OST) and Maintenance Surveillance (MSP) packages. The reviews verified that the equipment or systems were being tested as required by TS, the UFSAR, and procedural requirements. The inspectors also verified that the licensee established proper test conditions, that no equipment pre-conditioning activities occurred, and that acceptance criteria were met.
: [[TS]] [[, the]]
* On March 26, 1OST-13.7B, Rev. 4, "Containment Depressurization System Operating Surveillance Test" [in-service testing];
: [[UFS]] [[]]
* On April 14, 1OST-1.04A, Rev. 0, "Train B, CIA On-line Valve Relay Test" [isolation valve];
AR, and procedural requirements. The inspectors also verified that the licensee
* On April 15, 1OST-36.2, Rev. 51, "Diesel Generator No. 2 Monthly Test";
established proper test conditions, that no equipment pre-conditioning activities occurred,
* On April 19, 1BVT-1.21.2, Rev. 15, "Trevitest Method for Main Steam Safety Valve Setpoint Check";
and that acceptance criteria were met. * On March 26,
* On April 20, 1OST-36.04, Rev. 25, "Diesel Generator No. 2 Automatic Test";
: [[1OST]] [[-13.7B, Rev. 4, "Containment Depressurization System Operating Surveillance Test" [in-service testing]; * On April 14, 1]]
* On June 6, 1OST-15.1, Rev. 22, "[1CC-P-1A] Quarterly Test";
: [[OST]] [[-1.04A, Rev. 0, "Train B,]]
* On May 10, 1OST-47.2B, Rev. 8, "Containment Closeout Inspection"; and
: [[CIA]] [[On-line Valve Relay Test" [isolation valve]; * On April 15, 1]]
* On June 24, Unit 2, 2OST-6.2A, Rev. 27, "Computer Generated Reactor Coolant System Water Inventory Balance" [leak rate].
: [[OST]] [[-36.2, Rev. 51, "Diesel Generator No. 2 Monthly Test"; * On April 19,]]
 
: [[1BVT]] [[-1.21.2, Rev. 15, "Trevitest Method for Main Steam Safety Valve Setpoint Check"; * On April 20, 1]]
====b. Findings====
: [[OST]] [[-36.04, Rev. 25, "Diesel Generator No. 2 Automatic Test"; * On June 6,]]
No findings of significance were identified. 2.
: [[1OST]] [[-15.1, Rev. 22, "[1]]
 
: [[CC]] [[-P-1A] Quarterly Test"; * On May 10,]]
==RADIATION SAFETY==
: [[1OST]] [[-47.2B, Rev. 8, "Containment Closeout Inspection"; and * On June 24, Unit 2, 2]]
 
OST-6.2A, Rev. 27, "Computer Generated Reactor Coolant System Water Inventory Balance" [leak rate].
===Cornerstone:===
b. Findings No findings of significance were identified. 2.
Occupational Radiation Safety [OS]
: [[RADIAT]] [[]]
 
: [[ION]] [[]]
2OS1 Access Control to Radiologically Significant Areas (71121.01)
: [[SAFETY]] [[Cornerstone: Occupational Radiation Safety []]
 
OS]
====a. Inspection Scope====
2OS1 Access Control to Radiologically Significant Areas (71121.01) a. Inspection Scope (10 samples) During the period April 27 - 30, the inspector conducted the following activities to verify
(10 samples)
that the licensee was properly implementing physical, administrative, and engineering
During the period April 27 - 30, the inspector conducted the following activities to verify that the licensee was properly implementing physical, administrative, and engineering controls for access to locked high radiation areas, and other radiologically controlled areas during the Unit 1 refueling outage. Implementation of these controls was reviewed against the criteria contained in 10 CFR 20, relevant TS, and the licensee's procedures.
controls for access to locked high radiation areas, and other radiologically controlled
 
areas during the Unit 1 refueling outage. Implementation of these controls was reviewed
This inspection activity represents the completion of ten (10) samples relative to this inspection area.
against the criteria contained in
 
: [[10 CFR]] [[20, relevant]]
Plant Walkdown and Radiation Work Permits (RWP) Reviews
TS, and the licensee's procedures.
* The inspector toured accessible radiologically controlled areas in the Unit 1 reactor building containment (RBC), primary auxiliary building, and radwaste building and with the assistance of a radiation protection technician, performed independent radiation surveys of selected areas to confirm the accuracy of survey data, and the adequacy of postings. Radiation protection technicians were questioned regarding their knowledge of plant radiological conditions for selected jobs, and the associated controls.
Enclosure This inspection activity represents the completion of ten (10) samples relative to this inspection area. Plant Walkdown and Radiation Work Permits (RWP) Reviews * The inspector toured accessible radiologically controlled areas in the Unit 1 reactor building containment (RBC), primary auxiliary building, and radwaste building and with the assistance of a radiation protection technician, performed independent
* The inspector identified radiologically significant jobs being performed in the Unit 1 RBC. The inspector reviewed the applicable RWPs, ALARA Plans (AP), and the electronic dosimeter dose/dose rate set points, for the associated tasks, to determine if the radiological controls were acceptable and if the set points were consistent with plant policy. Jobs reviewed included steam generator sludge lancing (RWP 109-4015, AP 09-1-24), insulation removal/replacement (RWP 109-4032, AP 09-1-29),
radiation surveys of selected areas to confirm the accuracy of survey data, and the
remove/replace core exit thermocouples (RWP 109-4019, 09-1-26), and in-service inspections (RWP 109-4023, AP 09-1-29).
adequacy of postings. Radiation protection technicians were questioned regarding
* For the jobs reviewed, the inspector determined that there were no significant dose gradients requiring relocation of dosimetry. The inspector determined that tele-dosimetry was extensively used to monitor and control worker exposure for dose intensive jobs.
their knowledge of plant radiological conditions for selected jobs, and the associated
* There were no current radiation work permits for airborne radioactivity areas with the potential for individual worker internal exposures to exceed 50 mrem during the 1R19 outage. The inspector reviewed air sampling records for ongoing jobs to confirm that airborne contamination was insignificant.
controls. * The inspector identified radiologically significant jobs being performed in the Unit
* The inspector evaluated the effectiveness of contamination controls by reviewing personnel contamination event reports (and related condition reports), and observing practices at various work locations in the RBC and at the step off pad.
: [[1 RBC.]] [[The inspector reviewed the applicable]]
 
: [[RWP]] [[s,]]
High Radiation Area and Very High Radiation Area Controls
: [[ALARA]] [[Plans (]]
* The inspector reviewed procedures related to the control of high dose rate, high radiation area and very high radiation areas. The inspector discussed these procedures with Radiation Protection Supervision to determine that any changes made to these procedures did not reduce safety measures.
AP), and the
* Keys to locked high radiation areas (LHRA) located in Unit 1 were inventoried, and accessible LHRAs were verified to be properly secured and posted during plant tours.
electronic dosimeter dose/dose rate set points, for the associated tasks, to determine
* The inspector reviewed the preparations made for various potentially high dose rate jobs including removal of core exit thermocouples, and insulation modifications made to various systems in the RBC. Included in this review were evaluating the effectiveness of contamination control measures, source term controls, and use of temporary shielding.
if the radiological controls were acceptable and if the set points were consistent with
 
plant policy. Jobs reviewed included steam generator sludge lancing (RWP 109-
Radiation Worker and Radiation Protection Technician Performance
4015,
* During tours of radiologically controlled areas in the Unit 1 RBC, the inspector questioned radiation workers and radiation protection technicians regarding the radiological conditions at the work site and the radiological controls that applied to their task. Additionally, radiologically-related condition reports, including dose/dose rate alarm reports, were reviewed to evaluate if the incidents were caused by repetitive radiation worker or technician errors and to determine if an observable pattern traceable to a similar cause was evident.
: [[AP]] [[09-1-24), insulation removal/replacement (]]
* The inspector attended the pre-job RWP briefings for a spent resin transfer, and for steam generator foreign object search and retrieval (FOSAR) to determine if workers were properly informed, including discussions of past operating experiences, identification of the radiological conditions associated with their tasks, electronic dosimetry dose/dose rate set points, and dose mitigation measures.
RWP 109-4032, AP 09-1-29),
 
remove/replace core exit thermocouples (RWP 109-4019, 09-1-26), and in-service
Problem Identification and Resolution
inspections (RWP 109-4023, AP 09-1-29). * For the jobs reviewed, the inspector determined that there were no significant dose gradients requiring relocation of dosimetry. The inspector determined that tele-
* The inspectors evaluated the licensee's program for assuring that access controls to radiologically significant areas were effective and properly implemented by reviewing various Nuclear Oversight Field Observation Reports, radiation protection supervisory daily logs, and relevant condition reports. The inspector determined if problems were identified in a timely manner, that an extent of condition and cause evaluation were performed when appropriate, previous radiation surveys remained valid, and corrective actions were appropriate to preclude repetitive problems.
dosimetry was extensively used to monitor and control worker exposure for dose
 
intensive jobs. * There were no current radiation work permits for airborne radioactivity areas with the potential for individual worker internal exposures to exceed 50 mrem during the 1R19
====b. Findings====
outage. The inspector reviewed air sampling records for ongoing jobs to confirm that
No findings of significance were identified.
airborne contamination was insignificant. * The inspector evaluated the effectiveness of contamination controls by reviewing personnel contamination event reports (and related condition reports), and observing
 
practices at various work locations in the RBC and at the step off pad. High Radiation Area and Very High Radiation Area Controls * The inspector reviewed procedures related to the control of high dose rate, high radiation area and very high radiation areas. The inspector discussed these
2OS2 ALARA Planning and Controls (71121.02)
procedures with Radiation Protection Supervision to determine that any changes
 
made to these procedures did not reduce safety measures. * Keys to locked high radiation areas (LHRA) located in Unit 1 were inventoried, and accessible
====a. Inspection Scope====
: [[LH]] [[]]
(9 samples)
RAs were verified to be properly secured and posted during plant tours. * The inspector reviewed the preparations made for various potentially high dose rate jobs including removal of core exit thermocouples, and insulation modifications made
During the period April 27 - 30, the inspector conducted the following activities to verify that the licensee was properly implementing operational, engineering, and administrative controls to maintain personnel exposure as low as is reasonably achievable (ALARA) for activities performed in the 1R19 refueling outage. Implementation of these controls was reviewed against the criteria contained in 10 CFR 20, and the licensee's procedures.
to various systems in the RBC. Included in this review were evaluating the
 
effectiveness of contamination control measures, source term controls, and use of
This inspection activity represents the completion of nine (9) samples relative to this inspection area.
temporary shielding.
 
Enclosure  Radiation Worker and Radiation Protection Technician Performance * During tours of radiologically controlled areas in the Unit 1 RBC, the inspector questioned radiation workers and radiation protection technicians regarding the
Radiological Work Planning
radiological conditions at the work site and the radiological controls that applied to
* The inspector reviewed pertinent information regarding site cumulative exposure history, current exposure trends, and the ongoing exposure challenges for the Unit 1 outage. The inspector reviewed the 1R19 Outage ALARA Plan.
their task. Additionally, radiologically-related condition reports, including dose/dose
* The inspector reviewed the exposure status for tasks performed during the Unit 1 outage and compared actual exposure with forecasted estimates contained in various project ALARA Plans (AP). The inspector reviewed the Work-In-Progress ALARA reviews for those jobs whose actual dose approached 75% of the forecasted estimate. Outage jobs reviewed included scaffolding installation (AP 09-1-35),
rate alarm reports, were reviewed to evaluate if the incidents were caused by
insulation modifications (AP 09-01-33), reactor disassembly/reassembly (AP 09-1-25), routine valve work (AP 09-1-41), and replacing incore detectors (AP 09-1-19).
repetitive radiation worker or technician errors and to determine if an observable
* The inspector evaluated the departmental interfaces between radiation protection, operations, maintenance crafts, and engineering to identify missing ALARA program elements and interface problems. The evaluation was accomplished by interviewing site staff, reviewing outage Work-in-Progress reviews, attending a Station ALARA Committee (SAC) meeting, and reviewing SAC meeting minutes. The SAC meeting addressed planning for cutting/replacing a reactor coolant drain line (RC-41), and revising the exposure estimate for insulation modifications.
pattern traceable to a similar cause was evident. * The inspector attended the pre-job
 
: [[RWP]] [[briefings for a spent resin transfer, and for steam generator foreign object search and retrieval (]]
Verification of Dose Estimates
FOSAR) to determine if workers
* The inspector reviewed the assumptions and basis for the 1R19 outage ALARA plan. The inspector also reviewed the revisions made to various outage project dose estimates due to emergent work; e.g., insulation modifications (RWP 109-4048),
were properly informed, including discussions of past operating experiences,
authorized by the Station ALARA Committee.
identification of the radiological conditions associated with their tasks, electronic
* The inspector reviewed the licensee's procedures associated with monitoring and re-evaluating dose estimates when the forecasted cumulative exposure for tasks was approached and the implementation of these procedures during the outage. The inspector reviewed the exposures for the ten (10) workers who received the highest doses to confirm that no individual exceeded any regulatory limit.
dosimetry dose/dose rate set points, and dose mitigation measures. Problem Identification and Resolution * The inspectors evaluated the licensee's program for assuring that access controls to radiologically significant areas were effective and properly implemented by reviewing
 
various Nuclear Oversight Field Observation Reports, radiation protection supervisory
Job Site Inspections
daily logs, and relevant condition reports. The inspector determined if problems were
* The inspector reviewed the ALARA controls specified for transferring resin from CH-I-1A to a disposal container (RWP 109-0507,AP 09-1-58, procedure 1/2 -HPP-3.03.007), and attended the pre-job ALARA briefing. The inspector also reviewed the controls used for manually transferring a spent filter (CH-FL-2) to a storage drum (RWP 109-1020, AP 09-1-11, procedure 1/2 OM-18.4A.E), the trouble shooting plan for removing the filter when it became disengaged from the transfer grapple, and the post-job debrief.
identified in a timely manner, that an extent of condition and cause evaluation were
* During tours of the RBC, the inspector observed workers performing steam generator sludge lancing/FOSAR (RWP 109-4015), eddy current testing on the recirculation spray heat exchanger (RWP 109-4043), valve repairs, and de-mobilization activities. Workers were questioned regarding their knowledge of job site radiological conditions and ALARA measures applied to their tasks.
performed when appropriate, previous radiation surveys remained valid, and
 
corrective actions were appropriate to preclude repetitive problems.
Source Term Reduction and Control
b. Findings No findings of significance were identified.
* The inspector reviewed the status and historical trends for the Unit 1 source term. Through review of survey maps and interviews with the Senior Nuclear Specialist-ALARA, the inspector evaluated recent source term measurements and control strategies. Specific strategies being employed included use of macro-porous clean up resin, zinc addition, increased filtration flow, enhanced chemistry controls, system flushes, and temporary shielding.
: [[2OS]] [[2]]
 
ALARA Planning and Controls (71121.02)
Declared Pregnant Workers
a. Inspection Scope (9 samples) During the period April 27 - 30, the inspector conducted the following activities to verify
* The inspector reviewed the procedural controls for managing declared pregnant workers (DPW) and determined that no DPW was employed during the Unit 1 outage. Problem Identification and Resolution
that the licensee was properly implementing operational, engineering, and administrative
* The inspector reviewed elements of the licensee's corrective action program related to implementing the ALARA program to determine if problems were being entered into the program for timely resolution. Condition reports related to programmatic dose challenges, personnel contaminations, and the effectiveness in predicting and controlling worker exposure were reviewed.
controls to maintain personnel exposure as low as is reasonably achievable (ALARA) for
activities performed in the 1R19 refueling outage. Implementation of these controls was
reviewed against the criteria contained in 10 CFR 20, and the licensee's procedures.
This inspection activity represents the completion of nine (9) samples relative to this
inspection area. Radiological Work Planning * The inspector reviewed pertinent information regarding site cumulative exposure history, current exposure trends, and the ongoing exposure challenges for the Unit 1
outage. The inspector reviewed the 1R19 Outage
: [[ALA]] [[]]
RA Plan. * The inspector reviewed the exposure status for tasks performed during the Unit 1 outage and compared actual exposure with forecasted estimates contained in
Enclosure various project
: [[ALARA]] [[Plans (]]
: [[AP]] [[). The inspector reviewed the Work-In-Progress]]
: [[ALA]] [[]]
RA reviews for those jobs whose actual dose approached 75% of the forecasted
estimate. Outage jobs reviewed included scaffolding installation (AP 09-1-35),
insulation modifications (AP 09-01-33), reactor disassembly/reassembly (AP 09-1-
25), routine valve work (AP 09-1-41), and replacing incore detectors (AP 09-1-19). * The inspector evaluated the departmental interfaces between radiation protection, operations, maintenance crafts, and engineering to identify missing
: [[ALA]] [[]]
RA program
elements and interface problems. The evaluation was accomplished by interviewing
site staff, reviewing outage Work-in-Progress reviews, attending a Station
: [[ALA]] [[]]
: [[RA]] [[Committee (SAC) meeting, and reviewing]]
: [[SAC]] [[meeting minutes. The]]
SAC meeting
addressed planning for cutting/replacing a reactor coolant drain line (RC-41), and
revising the exposure estimate for insulation modifications. Verification of Dose Estimates * The inspector reviewed the assumptions and basis for the 1R19 outage
: [[ALA]] [[]]
RA plan. The inspector also reviewed the revisions made to various outage project dose
estimates due to emergent work; e.g., insulation modifications (RWP 109-4048),
authorized by the Station
: [[ALA]] [[]]
RA Committee. * The inspector reviewed the licensee's procedures associated with monitoring and re-evaluating dose estimates when the forecasted cumulative exposure for tasks was
approached and the implementation of these procedures during the outage. The
inspector reviewed the exposures for the ten (10) workers who received the highest
doses to confirm that no individual exceeded any regulatory limit. Job Site Inspections * The inspector reviewed the
: [[ALARA]] [[controls specified for transferring resin from]]
CH-I-1A to a disposal container (RWP 109-0507,AP 09-1-58, procedure 1/2 -HPP-
3.03.007), and attended the pre-job
: [[ALA]] [[]]
RA briefing. The inspector also reviewed the
controls used for manually transferring a spent filter (CH-FL-2) to a storage drum  
(RWP 109-1020,
: [[AP]] [[09-1-11, procedure 1/2]]
OM-18.4A.E), the trouble shooting plan
for removing the filter when it became disengaged from the transfer grapple, and the
post-job debrief.  
* During tours of the
: [[RBC]] [[, the inspector observed workers performing steam generator sludge lancing/]]
FOSAR (RWP 109-4015), eddy current testing on the recirculation
spray heat exchanger (RWP 109-4043), valve repairs, and de-mobilization activities. Workers were questioned regarding their knowledge of job site radiological
conditions and
: [[ALA]] [[]]
: [[RA]] [[measures applied to their tasks. Source Term Reduction and Control * The inspector reviewed the status and historical trends for the Unit 1 source term. Through review of survey maps and interviews with the Senior Nuclear Specialist-]]
: [[ALA]] [[]]
RA, the inspector evaluated recent source term measurements and control
strategies. Specific strategies being employed included use of macro-porous clean
Enclosure up resin, zinc addition, increased filtration flow, enhanced chemistry controls, system flushes, and temporary shielding. Declared Pregnant Workers * The inspector reviewed the procedural controls for managing declared pregnant workers (DPW) and determined that no DPW was employed during the Unit 1
outage. Problem Identification and Resolution * The inspector reviewed elements of the licensee's corrective action program related to implementing the
: [[ALA]] [[]]
RA program to determine if problems were being entered
into the program for timely resolution. Condition reports related to programmatic
dose challenges, personnel contaminations, and the effectiveness in predicting and
controlling worker exposure were reviewed.
b. Findings  No findings of significance were identified. 4.
: [[OTHER]] [[]]
ACTIVITIES [OA]
4OA1 Performance Indicator Verification (71151)
a. Inspection Scope (6 samples total)  The inspectors sampled licensee submittals for Performance Indicators (PI) listed below
for both Unit 1 and Unit 2 to verify accuracy of the data recorded from April 2007 through
June 2009. The inspectors reviewed Licensee Event Reports, condition reports, portions
of various plant operating logs and reports, and PI data developed from monthly
operating reports. Methods for compiling and reporting the
: [[PI]] [[s were discussed with cognizant engineering and licensing personnel. To verify the accuracy of the]]
PI data
reported during this period, PI definitions and guidance contained in Nuclear Energy
Institute (NEI) 99-02, "Regulatory Assessment Indicator Guideline," Revision 5, were
used for each data element.
Cornerstone: Mitigating Systems (2 samples)  * Unit 1 and 2 Safety System Functional Failure [MS05]
Cornerstone: Barrier Integrity (4 samples)  * Unit 1 and 2 Reactor Coolant System Activity  [BI01] * Unit 1 and 2 Reactor Coolant System Leak Rate  [BI02]    b. Findings  No findings of significance were identified.  


Enclosure 4OA2 Problem Identification and Resolution (71152 - 2 samples total)
====b. Findings====
.1 Daily Review of Problem Identification and Resolution
No findings of significance were identified.
a. Inspection Scope
 
==OTHER ACTIVITIES==
[OA]
{{a|4OA1}}
==4OA1 Performance Indicator Verification==
{{IP sample|IP=IP 71151}}
 
====a. Inspection Scope====
(6 samples total)
The inspectors sampled licensee submittals for Performance Indicators (PI) listed below for both Unit 1 and Unit 2 to verify accuracy of the data recorded from April 2007 through June 2009. The inspectors reviewed Licensee Event Reports, condition reports, portions of various plant operating logs and reports, and PI data developed from monthly
 
operating reports. Methods for compiling and reporting the PIs were discussed with cognizant engineering and licensing personnel. To verify the accuracy of the PI data reported during this period, PI definitions and guidance contained in Nuclear Energy Institute (NEI) 99-02, "Regulatory Assessment Indicator Guideline," Revision 5, were used for each data element.
 
===Cornerstone:===
Mitigating Systems (2 samples)
* Unit 1 and 2 Safety System Functional Failure [MS05]
 
===Cornerstone:===
Barrier Integrity (4 samples)
* Unit 1 and 2 Reactor Coolant System Activity  [BI01]
* Unit 1 and 2 Reactor Coolant System Leak Rate  [BI02]
 
====b. Findings====
No findings of significance were identified.
 
{{a|4OA2}}
==4OA2 Problem Identification and Resolution (71152 - 2 samples total)==
 
===.1 Daily Review of Problem Identification and Resolution===
 
====a. Inspection Scope====
As required by Inspection Procedure 71152, "Identification and Resolution of Problems,"
As required by Inspection Procedure 71152, "Identification and Resolution of Problems,"
and in order to help identify repetitive equipment failures or specific human performance
and in order to help identify repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed a daily screening of items entered into FENOC's corrective action program. This review was accomplished by reviewing summary lists of each CR, attending screening meetings, and accessing FENOC's computerized CR database.
issues for follow-up, the inspectors performed a daily screening of items entered into
: [[FEN]] [[]]
OC's corrective action program. This review was accomplished by reviewing
summary lists of each
: [[CR]] [[, attending screening meetings, and accessing]]
FENOC's
computerized CR database.
b. Findings  No findings of significance were identified.
.2 Annual Sample: Review of Final Cause and Corrective Actions of Inadvertent Unlatch of a Control Rod Drive Shaft during Refueling 2R13
a. Inspection Scope (1 sample)  The inspectors selected
: [[CR]] [[08-39693 as a problem identification and resolution (]]
PI&R)
sample for a detailed follow-up review. CR 08-39693 documented on May 2, 2008, an
inadvertent unlatching of a control rod drive shaft during its transfer from its storage
location to its core location by vendor personnel after planned split pin replacements.
The tool used in the drive shaft installation was specific to the split pin replacement
project. Review of the initial event is documented in report 05000412 / 2008003.  


The inspectors reviewed the vendor apparent cause and assessed
====b. Findings====
: [[FEN]] [[]]
No findings of significance were identified.
OC's cause
analysis, extent of condition, operability determination, and prioritization and timeliness of corrective actions to prevent recurrence. Documents reviewed for this inspection are
located in the Attachment.
b. Findings and Observations  No findings of significance were identified.  


The inspectors determined that
===.2 Annual Sample: Review of Final Cause and Corrective Actions of Inadvertent Unlatch of a Control Rod Drive Shaft during Refueling 2R13===
: [[FEN]] [[]]
OC properly evaluated the degraded condition and
implemented appropriate immediate and long term corrective actions. The CR was
complete and included cause evaluations by
: [[FEN]] [[]]
OC and the vendor. No human
performance deficiencies were noted. It was determined that the handing tool is not fail-
safe and can unlatch if the drive shaft weight is relieved by interference with a guide
card. The licensee discontinued use of the vendor's special tool during the issue and
has revised applicable procedures to prevent future use. 
.3 Annual Sample: Review of Submerged Safety Related Cables    a. Inspection Scope (1 sample) 


Enclosure The inspectors selected
====a. Inspection Scope====
: [[CR]] [[08-42380 as a]]
(1 sample)
PI&R sample for a detailed follow-up review. CR 08-42380 documented the identification of safety related cables found submerged in
The inspectors selected CR 08-39693 as a problem identification and resolution (PI&R)sample for a detailed follow-up review. CR 08-39693 documented on May 2, 2008, an inadvertent unlatching of a control rod drive shaft during its transfer from its storage location to its core location by vendor personnel after planned split pin replacements.
water on June 25, 2008 for an indefinite period of time. The issue was identified during
routine manhole inspections. The inspectors assessed
: [[FEN]] [[]]
OC's problem identification
threshold, operability determination, extent of condition review, and the prioritization and timeliness of corrective actions to determine whether
: [[FEN]] [[]]
OC was appropriately
identifying, characterizing, and correcting problems associated with these issues and
whether the planned or completed corrective actions were appropriate to prevent
recurrence. Additionally, the inspectors observed manhole and cable inspections on
June 9-10, 2009 and interviewed engineering personnel. The inspectors reviewed the
specification, testing and long term moisture resistance qualification report for the subject
cables. Specific documents reviewed are listed in the attachment to this report.
b. Findings and Observations  Introduction:  The inspectors identified a non-cited violation (NCV) of
: [[10CFR]] [[Part 50, Appendix B, Criterion]]
: [[III]] [[, "Design Control," in that]]
: [[FEN]] [[]]
OC did not maintain safety related cables in an environment for which they were designed. The licensee failed to
demonstrate that the cables are qualified for continuous submerged conditions, and that
they will remain operable, although the cables are presently operable.
Description:  Safety related and non-safety related power and control cables may be submerged in water on a continuous basis. The affected cables included cables from
the Unit 1 River Water and Unit 2 Service Water from the Main Intake Structure carrying
power to the Class 1E load through electrical manholes
: [[1EMH]] [[-8A and 1]]
EMH-8B.  


A review of the licensing basis and licensee documentation reveals the cables are
The tool used in the drive shaft installation was specific to the split pin replacement project. Review of the initial event is documented in report 05000412 / 2008003.
selected and purchased for dry, wet, and immersed in water conditions. The inspectors
 
determined, after discussions with additional NRC specialists, that this does not include
The inspectors reviewed the vendor apparent cause and assessed FENOC's cause analysis, extent of condition, operability determination, and prioritization and timeliness of corrective actions to prevent recurrence. Documents reviewed for this inspection are located in the Attachment.
continuous submerged conditions. The inspectors reviewed the specifications used to
 
purchase these cables and noted that the subject cables are not designed for continuous
====b. Findings and Observations====
submergance.  
No findings of significance were identified.
 
The inspectors determined that FENOC properly evaluated the degraded condition and implemented appropriate immediate and long term corrective actions. The CR was complete and included cause evaluations by FENOC and the vendor. No human performance deficiencies were noted. It was determined that the handing tool is not fail-safe and can unlatch if the drive shaft weight is relieved by interference with a guide card. The licensee discontinued use of the vendor's special tool during the issue and has revised applicable procedures to prevent future use.
 
===.3 Annual Sample: Review of Submerged Safety Related Cables===
 
====a. Inspection Scope====
(1 sample)
The inspectors selected CR 08-42380 as a PI&R sample for a detailed follow-up review. CR 08-42380 documented the identification of safety related cables found submerged in water on June 25, 2008 for an indefinite period of time. The issue was identified during routine manhole inspections. The inspectors assessed FENOC's problem identification threshold, operability determination, extent of condition review, and the prioritization and timeliness of corrective actions to determine whether FENOC was appropriately identifying, characterizing, and correcting problems associated with these issues and whether the planned or completed corrective actions were appropriate to prevent recurrence. Additionally, the inspectors observed manhole and cable inspections on June 9-10, 2009 and interviewed engineering personnel. The inspectors reviewed the specification, testing and long term moisture resistance qualification report for the subject cables. Specific documents reviewed are listed in the attachment to this report.
 
====b. Findings and Observations====
 
=====Introduction:=====
The inspectors identified a non-cited violation (NCV) of 10CFR Part 50, Appendix B, Criter ion III, "Design Control," in that FENOC did not maintain safety related cables in an environment for which they were designed. The licensee failed to demonstrate that the cables are qualified for continuous submerged conditions, and that they will remain operabl e, although t he cables are presently operable.
 
=====Description:=====
Safety related and non-safety related power and control cables may be submerged in water on a continuous basis. The affected cables included cables from the Unit 1 River Water and Unit 2 Service Water from the Main Intake Structure carrying power to the Class 1E load through electrical manholes 1EMH-8A and 1EMH-8B.
 
A review of the licensing basis and licensee documentation reveals the cables are selected and purchased for dry, wet, and immersed in water conditions. The inspectors determined, after discussions with additional NRC specialists, that this does not include continuous submerged conditions. The inspectors reviewed the specifications used to purchase these cables and noted that the subject cables are not designed for continuous submergance.


The environmental conditions in the manholes can be dry, wet, and immersed in water.
The environmental conditions in the manholes can be dry, wet, and immersed in water.
A review of the licensee's underground cable duct drawings showed that the manholes
are constructed below grade and expected to accumulate water. However, the cables
can become continuously submerged in water if the accumulation is not managed or
manhole degraded conditions not effectively corrected. Presently, the licensee relies on
cable penetration seal integrity and manual dewatering of the manholes annually (for
1EMH-8A and 8B only) or biennially to manage water accumulation. The most recent
inspection (June 9, 2009) of manholes identified approximately 2 feet of water in 1EMH-
8A and 11 feet of water in 1EMH-8B; conditions of apparent continuous submergence for
manhole 1EMH-8B cables. The licensee failed to ensure that the cables were
maintained in a design condition for the anticipated environmental conditions by not
thoroughly evaluating the effect of continuous cable submergence apparent in CRs
09-60591; 08-43594; 08-42380; 06-6305; 06-04144; 04-03545; 02-02348 and evaluating
the effectiveness of prior corrective actions.


The licensee had previously documented an engineering evaluation of cable suitability to submerged conditions (CR 02-02348, March 21, 2002) to address NRC Information
A review of the licensee's underground cable duct drawings showed that the manholes are constructed below grade and expected to accumulate water. However, the cables can become continuously submerged in water if the accumulation is not managed or manhole degraded conditions not effectively corrected. Presently, the licensee relies on cable penetration seal integrity and manual dewatering of the manholes annually (for 1EMH-8A and 8B only) or biennially to manage water accumulation. The most recent inspection (June 9, 2009) of manholes identified approximately 2 feet of water in 1EMH-8A and 11 feet of water in 1EMH-8B; conditions of apparent continuous submergence for manhole 1EMH-8B cables. The licensee failed to ensure that the cables were maintained in a design condition for the anticipated environmental conditions by not thoroughly evaluating the effect of continuous cable submergence apparent in CRs 09-60591; 08-43594; 08-42380; 06-6305; 06-04144; 04-03545; 02-02348 and evaluating the effectiveness of prior corrective actions.
Notice 2002-12, Submerged Safety-Related Electrical Cables. The licensee concluded
 
Enclosure that based on cable construction, qualification testing performed, and operational performance, the cables in manholes 1EMH-8A and 8B were acceptable. This
The licensee had previously doc umented an engineering evaluation of cable suitability to submerged conditions (CR 02-02348, March 21, 2002) to address NRC Information Notice 2002-12, Submerged Safety-Related Electrical Cables. The licensee concluded that based on cable construction, qualification testing performed, and operational performance, the cables in manholes 1EMH-8A and 8B were acceptable. This evaluation had also been the basis for subsequent evaluations for as-found manhole conditions. Corrective actions were taken to annually inspect and dewater the manholes and address as-found degraded conditions, however the licensee has not adequately addressed the apparent continuous submergence of safety related cables in the subject manholes.
evaluation had also been the basis for subsequent evaluations for as-found manhole
 
conditions. Corrective actions were taken to annually inspect and dewater the manholes
The licensee has pumped down water from the manholes to minimize water, and
and address as-found degraded conditions, however the licensee has not adequately
 
addressed the apparent continuous submergence of safety related cables in the subject
inspected the cables, seals, and tray supports. An immediate operability assessment was also performed for as found conditions and CRs written (09-60316; 09-60445; 09-60591). The inspectors questioned the licensee on the need to re-evaluate the frequency of manhole inspections, based on as-found conditions.
manholes.  
 
A review of the licensee's response to NRC Generic Letter 2007-01, "Inaccessible or Underground Power Cable Failures that Disable Accident Mitigation Systems or Cause Plant Transients," did not identify any past cable failures at Beaver Valley.
 
=====Analysis:=====
Failure to maintain safety related cables in an environment for which they were designed is considered a performance deficiency. The inspectors determined that the performance deficiency was not similar to the examples for minor deficiencies contained in IMC 0612, Appendix E, "Examples of Minor Issues". The finding was more than minor in accordance with IMC 0612, Appendix B (Section 1-3), "Issue Screening," because if left uncorrected, the performance deficiency has the potential to lead to a more significant safety concern. Traditional enforcement does not apply since there were no actual safety consequences or potential for impacting the NRC's regulatory function, and the finding did not have willful aspects.
 
In accordance with IMC 0609.04 (Table 4a), "Phase 1 - Initial Screening and Characterization of Findings," the finding was determined to be of very low safety significance (Green) because the finding was not a design or qualification deficiency which resulted in a loss of operability or functionality, did not represent a loss of system safety function, did not represent an actual loss of safety function of a single train for greater than its technical specification allowed outage time, did not represent an actual loss of safety function of one or more non-technical specification trains of equipment designated as risk-significant for greater than 24 hours, and was not potentially risk significant due to a seismic, flooding or severe weather initiating event.
 
The performance deficiency had a cross-cutting aspect in the area of Problem Identification and Resolution, Corrective Action Program, because the licensee did not thoroughly evaluate problems such as the resolutions, address causes, and evaluate the effectiveness of corrective actions [P.1 (c)].
 
=====Enforcement:=====
Title 10 CFR Part 50, Appendix B, Crit erion III, "Des ign Control," requires, in part, that measures shall be established to ensure that applicable regulatory requirements and the design basis are correctly translated into specifications, drawings, procedures, and instructions. Contrary to the above, FENOC did not maintain safety related cables in an environment for which they were designed. The issue was entered into the licensee's corrective action program (CR 09-60496) to initiate a review of the current manhole and cable monitoring programs, and to initiate long-term corrective actions. Because this finding was of very low safety significance, and it was entered into the licensee's corrective action program, this violation is being treated as an NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy. (NCV 05000334, 412/2009003-02, Continuously Submerged Cables Design Deficiency)
 
{{a|4OA3}}
==4OA3 Followup of Events and Notices of Enforcement Discretion (71153 - 7 samples total)==
 
===.1 Plant Event Review===


The licensee has pumped down water from the manholes to minimize water, and
====a. Inspection Scope====
inspected the cables, seals, and tray supports. An immediate operability assessment was also performed for as found conditions and CRs written (09-60316; 09-60445;
(6 samples)
09-60591). The inspectors questioned the licensee on the need to re-evaluate the
For the plant events below, the inspectors reviewed and/or observed plant parameters, reviewed personnel performance, and evaluated performance of mitigating systems.
frequency of manhole inspections, based on as-found conditions.  


A review of the licensee's response to NRC Generic Letter 2007-01, "Inaccessible or
The inspectors communicated the plant events to regional personnel and compared the event details with criteria contained in IMC 0309, "Reactive Inspection Decision Basis for Reactors," for consideration of additional reactive inspection activities. The inspectors reviewed FENOC's follow-up actions related to the events to assure that appropriate corrective actions were implemented commensurate with their safety significance.
Underground Power Cable Failures that Disable Accident Mitigation Systems or Cause
Plant Transients," did not identify any past cable failures at Beaver Valley.  


Analysis:  Failure to maintain safety related cables in an environment for which they were designed is considered a performance deficiency. The inspectors determined that the
Documents reviewed during the inspection are listed in the Attachment.
performance deficiency was not similar to the examples for minor deficiencies contained
* Unit 1: On April 20, 2009, main feedwater isolation (P14 actuation on high 'B' steam generator water level) during plant shutdown for refueling outage 1R19.
in IMC 0612, Appendix E, "Examples of Minor Issues". The finding was more than minor
in accordance with IMC 0612, Appendix B (Section 1-3), "Issue Screening," because if
left uncorrected, the performance deficiency has the potential to lead to a more
significant safety concern. Traditional enforcement does not apply since there were no
actual safety consequences or potential for impacting the NRC's regulatory function, and
the finding did not have willful aspects.


In accordance with IMC 0609.04 (Table 4a), "Phase 1 - Initial Screening and
The high steam generator water level was caused by a failed main feedwater bypass regulating valve (1FW-489) controller, causing it to inadvertently fully open. Operators responded appropriately and mitigating systems performed as designed. The licensee documented this issue in CR 09-57474. This issue was also reviewed under NRC OpESS FY2009-02, "Negative Trend and Recurring Events Involving Feedwater Systems;"
Characterization of Findings," the finding was determined to be of very low safety
* Unit 1: On April 20, 2009, invalid actuation of the steam-driven auxiliary feedwater pump (FW-P-2) during plant shutdown for refueling outage 1R19. An apparent failed solid state protection relay caused one of two steam admission valves (TV-1MS-105B) to open, causing the pump to inject. The auxiliary feedwater flow control system responded appropriately to mitigate the effect on plant cooldown.
significance (Green) because the finding was not a design or qualification deficiency
 
which resulted in a loss of operability or functionality, did not represent a loss of system safety function, did not represent an actual loss of safety function of a single train for
The licensee documented this issue in CR 09-57499. This issue was also reviewed under NRC OpESS FY2009-02, "Negative Trend and Recurring Events Involving Feedwater Systems;"
greater than its technical specification allowed outage time, did not represent an actual
* Unit 1: On April 23, 2009, identification of a degraded containment liner plate during a planned visual inspection in refueling outage 1R19. The degradation was repaired and declared operable on May 7, 2009. The licensee documented this issue in CRs 09-57589 and 09-57762. Also see section 1R08, "Inservice Inspection."  This issue is documented in NRC Inspection Report 05000334/2009006 (ADAMS ML091870328, on July 6, 2009);
loss of safety function of one or more non-technical specification trains of equipment
* Unit 1: On April 26, 2009, identification of two circumferential ultrasonic examination indications on base material of a 2 inch reactor coolant loop drain line (BV-1RC-41) on the 'A' loop hot leg. The drain line material was replaced and returned to service. Also see section 1R08, "Inservice Inspection.The licensee documented this issue in CR 09-58004;
designated as risk-significant for greater than 24 hours, and was not potentially risk
* Unit 1: On May 6, 2009, inadvertent train 'A' safety injection signal was generated, while in mode 5, due to a faulty safety injection block switch.
significant due to a seismic, flooding or severe weather initiating event. The performance deficiency had a cross-cutting aspect in the area of Problem
Identification and Resolution, Corrective Action Program, because the licensee did not
thoroughly evaluate problems such as the resolutions, address causes, and evaluate the
effectiveness of corrective actions [P.1 (c)].  


Enforcement:  Title
: [[10 CFR]] [[Part 50, Appendix B, Criterion]]
III, "Design Control," requires, in part, that measures shall be established to ensure that applicable regulatory
requirements and the design basis are correctly translated into specifications, drawings,
procedures, and instructions. Contrary to the above,
: [[FEN]] [[]]
OC did not maintain safety
related cables in an environment for which they were designed. The issue was entered
into the licensee's corrective action program (CR 09-60496) to initiate a review of the
current manhole and cable monitoring programs, and to initiate long-term corrective
actions. Because this finding was of very low safety significance, and it was entered into
Enclosure the licensee's corrective action program, this violation is being treated as an
: [[NCV]] [[, consistent with Section]]
: [[VI.A.]] [[1 of the]]
: [[NRC]] [[Enforcement Policy. (]]
NCV 05000334, 412/2009003-02, Continuously Submerged Cables Design Deficiency)  4OA3 Followup of Events and Notices of Enforcement Discretion (71153 - 7 samples total) 
.1 Plant Event Review  a. Inspection Scope (6 samples)  For the plant events below, the inspectors reviewed and/or observed plant parameters,
reviewed personnel performance, and evaluated performance of mitigating systems.
The inspectors communicated the plant events to regional personnel and compared the
event details with criteria contained in IMC 0309, "Reactive Inspection Decision Basis for
Reactors," for consideration of additional reactive inspection activities. The inspectors
reviewed
: [[FEN]] [[]]
OC's follow-up actions related to the events to assure that appropriate
corrective actions were implemented commensurate with their safety significance.
Documents reviewed during the inspection are listed in the Attachment.
* Unit 1: On April 20, 2009, main feedwater isolation (P14 actuation on high 'B' steam generator water level) during plant shutdown for refueling outage 1R19.
The high steam generator water level was caused by a failed main feedwater
bypass regulating valve (1FW-489) controller, causing it to inadvertently fully
open. Operators responded appropriately and mitigating systems performed as
designed. The licensee documented this issue in CR 09-57474. This issue was
also reviewed under
: [[NRC]] [[Op]]
ESS FY2009-02, "Negative Trend and Recurring
Events Involving Feedwater Systems;"  * Unit 1: On April 20, 2009, invalid actuation of the steam-driven auxiliary feedwater pump (FW-P-2) during plant shutdown for refueling outage 1R19. An apparent
failed solid state protection relay caused one of two steam admission valves (TV-
1MS-105B) to open, causing the pump to inject. The auxiliary feedwater flow control system responded appropriately to mitigate the effect on plant cooldown.
The licensee documented this issue in CR 09-57499. This issue was also
reviewed under
: [[NRC]] [[Op]]
ESS FY2009-02, "Negative Trend and Recurring Events
Involving Feedwater Systems;"  * Unit 1: On April 23, 2009, identification of a degraded containment liner plate during a planned visual inspection in refueling outage 1R19. The degradation
was repaired and declared operable on May 7, 2009. The licensee documented
this issue in CRs 09-57589 and 09-57762. Also see section 1R08, "Inservice
Inspection."  This issue is documented in NRC Inspection Report
05000334/2009006 (ADAMS ML091870328, on July 6, 2009);  * Unit 1: On April 26, 2009, identification of two circumferential ultrasonic examination indications on base material of a 2 inch reactor coolant loop drain
line (BV-1RC-41) on the 'A' loop hot leg. The drain line material was replaced
and returned to service. Also see section 1R08, "Inservice Inspection."  The
licensee documented this issue in CR 09-58004;
Enclosure * Unit 1: On May 6, 2009, inadvertent train 'A' safety injection signal was generated, while in mode 5, due to a faulty safety injection block switch.
Operators responded appropriately and no safety injection actually occurred.
Operators responded appropriately and no safety injection actually occurred.
Faulty switches were replaced. The licensee documented this issue in CR 09-
58765; and  * Unit 1 and Unit 2: On June 18, 2009, at 9:39 p.m., a dual-unit Unusual Event (UE) was declared in response to a fire alarm and CO2 system actuation in the
Emergency Response Facility (ERF) substation. The licensee entered emergency action level (EAL) 4.1. The onsite fire brigade responded and no fire
was discovered, and determined there was a spurious actuation of the CO2
system. The UE was terminated at 10:36 p.m. The licensee is still investigating
the cause, but is preliminarily attributed to a fire protection panel fault. The
licensee documented this issue in CR 09-60763.
b. Findings
No findings of significance were identified.
.2 Review of Licensee Event Reports (LERs) (1 sample)  (Closed) LER 05000334/2009-001-00:  Surveillance Test Inadvertently Violates Technical Specification 3.6.1 for Containment Operability.


During a planned surveillance flow test on one of two outside recirculation spray system (RSS) pumps while in Mode 1, the suction and discharge containment isolation valves on
Faulty switches were replaced. The licensee documented this issue in CR 09-58765; and
the RSS train of piping were closed, but not de-energized. These valves receive an
* Unit 1 and Unit 2: On June 18, 2009, at 9:39 p.m., a dual-unit Unusual Event (UE) was declared in response to a fire alarm and CO2 system actuation in the Emergency Response Facility (ERF) substation. T he licensee entered emergency action level (EAL) 4.1. The onsite fire brigade responded and no fire was discovered, and determined there was a spurious actuation of the CO2 system. The UE was terminated at 10:36 p.m. The licensee is still investigating the cause, but is preliminarily attributed to a fire protection panel fault. The licensee documented this issue in CR 09-60763
auto-open signal during a phase 'B' containment isolation. After the test, when the pump
.
casing drain valve was opened to drain the system to restore to a normal configuration,
 
the operations crew realized that the containment isolation valves needed to be de-
====b. Findings====
energized in order to maintain containment operability. This condition existed in excess of seven hours, twice, during filling and draining sequences. This is contrary to the requirement in TS 3.6.1, "Containment". The crew immediately de-energized the
No findings of significance were identified.
affected valves.       The inspectors reviewed the LER, verified the appropriateness of corrective actions and
 
extent of condition reviews, interviewed engineers and licensed operators, and
===.2 Review of Licensee Event Reports (LERs) (1 sample)===
completed a plant walkdown with
 
: [[FEN]] [[]]
(Closed) LER 05000334/2009-001-00:  Surveillance Test Inadvertently Violates Technical Specification 3.6.1 for Containment Operability.
OC engineers to identify the pump casing drain
 
valve. Corrective actions include revising affected procedures to properly include TS
During a planned surveillance flow test on one of two outside re circulation spray system (RSS) pumps while in Mode 1, the suction and discharge containment isolation valves on the RSS train of piping were closed, but not de-energized. These valves receive an auto-open signal during a phase 'B' containment isolation. After the test, when the pump casing drain valve was opened to drain the system to restore to a normal configuration, the operations crew realized that the containment isolation valves needed to be de-energized in order to maintain containment operability. This condition existed in excess of seven hours, twice, during filling and draining sequences. This is contrary to the requirement in TS 3.6.1, "Containment". The crew immediately de-energized the affected valves.
3.6.1. The enforcement aspects of the violation are discussed in Section 4OA7,
 
Licensee Identified Violations. This
The inspectors reviewed the LER, verified the appropriateness of corrective actions and extent of condition reviews, interviewed engineers and licensed operators, and completed a plant walkdown with FENOC engineers to identify the pump casing drain valve. Corrective actions include revising affected procedures to properly include TS 3.6.1. The enforcement aspects of the violation are discussed in Section 4OA7, Licensee Identified Violations. This LER is closed.
: [[LER]] [[is closed. 4]]
{{a|4OA5}}
OA5 Other Activities .1 Quarterly Resident Inspector Observations of Security Personnel and Activities
==4OA5 Other Activities==
a. Inspection Scope During the inspection period, the inspectors conducted the following observations of
 
security force personnel and activities to ensure that the activities were consistent with
===.1 Quarterly Resident Inspector Observations of Security Personnel and Activities===
Enclosure licensee security procedures and regulatory requirements relating to nuclear plant security. These observations took place during both normal and off-normal plant working
 
hours. Specific examples include: * Observed operations within the central and secondary alarm stations; * Toured selected security towers and security officer response posts; * Observed security force shift turnover activities; and * Reviewed security logs and corrective action program documents which discussed security issues.
====a. Inspection Scope====
These quarterly resident inspector observations of security force personnel and activities did not constitute any additional inspection samples. Rather, they were considered an
During the inspection period, the inspectors conducted the following observations of security force personnel and activities to ensure that the activities were consistent with licensee security procedures and regulatory requirements relating to nuclear plant security. These observations took place during both normal and off-normal plant working hours. Specific examples include:
integral part of the inspectors' normal plant status review and inspection activities.
* Observed operations within the central and secondary alarm stations;
b. Findings
* Toured selected security towers and security officer response posts;
No findings of significance were identified.  
* Observed security force shift turnover activities; and
* Reviewed security logs and corrective action program documents which discussed security issues.
 
These quarterly resident inspector observations of security force personnel and activities did not constitute any additional inspection samples. Rather, they were considered an integral part of the inspectors' normal plant status review and inspection activities.


.2 TI 2515/172, Reactor Coolant System Dissimilar Metal Butt Welds (Unit 1)
====b. Findings====
a. Inspection Scope Temporary Instruction, TI 2515/172 provides for confirmation that owners of pressurized-
No findings of significance were identified.
water reactors (PWRs) have implemented the industry guidelines of the Materials
 
Reliability Program (MRP) -139 regarding nondestructive examination and evaluation of certain dissimilar metal (DM) welds in reactor coolant systems containing Alloy
===.2 TI 2515/172, Reactor Coolant System Dissimilar Metal Butt Welds (Unit 1)===
600/82/182. The TI requires documentation of specific questions in an inspection report.
 
The questions and responses were previously documented in NRC Inspection Report
====a. Inspection Scope====
05000334, 412/2008003, Attachment
Temporary Instruction, TI 2515/172 provides for confirmation that owners of pressurized-water reactors (PWRs) have implemented the industry guidelines of the Materials Reliability Program (MRP) -
: [[B.]] [[The hot and cold leg nozzle-to-safe end dissimilar metal (DM) welds of the "A" S/G were examined during this 1st period inspection interval (1R19 outage). These welds were Risk-Informed]]
139 regarding nondestructive examination and evaluation of certain dissimilar metal (DM) welds in reactor coolant systems containing Alloy 600/82/182. The TI requires documentation of specific questions in an inspection report.
: [[ISI]] [[]]
 
UT examined during 1R19. During the S/G replacement project 1R17,
The questions and responses were previously documented in NRC Inspection Report 05000334, 412/2008003, Attachment B.
these particular nozzle welds were replaced with Alloy 52 and are resistant to stress-
 
corrosion cracking and are considered Category "A" welds per MRP-139, Revision 1, and
The hot and cold leg nozzle-to-safe end dissimilar metal (DM) welds of the "A" S/G were examined during this 1 st period inspection interval (1R19 outage). These welds were Risk-Informed ISI UT examined during 1R19. During the S/G replacement project 1R17, these particular nozzle welds were replaced with Alloy 52 and are resistant to stress-corrosion cracking and are considered Category "A" welds per MRP-139, Revision 1, and therefore the required examinations are per ASME Section XI. ASME Section XI, Table IWB-2500-1, B5.70 requires a volumetric and surface exam once per interval of the dissimilar metal welds for the S/G cold and hot leg nozzle-to-safe end welds. The Risk-Informed examination of these DM welds was only a UT examination (no surface exam) since these welds were selected in a particular piping segment per the Risk-Informed, ISI program that supersedes the ASME Section XI Code exam. The inspector reviewed the manual UT examination data records of the "A" S/G cold and hot leg nozzle-to-safe-end DM welds RC-E-1A-N11 and RC-E-1A-N12.
therefore the required examinations are per
 
: [[ASME]] [[Section]]
====b. Findings====
: [[XI.]] [[]]
No findings of significance were identified.
: [[ASME]] [[Section]]
{{a|4OA6}}
XI, Table
==4OA6 Meetings, Including Exit==
IWB-2500-1, B5.70 requires a volumetric and surface exam once per interval of the
 
dissimilar metal welds for the S/G cold and hot leg nozzle-to-safe end welds. The
===.1 Access Control / ALARA Planning and Control===
Risk-Informed examination of these
 
: [[DM]] [[welds was only a]]
The inspector presented the inspection results of 2S01 and 2S02 to Mr. Kevin Ostrowski, Director of Site Operations, and other members of FENOC staff, at the conclusion of the inspection on April 30, 2009. No proprietary information is presented in this report.
UT examination (no surface
 
exam) since these welds were selected in a particular piping segment per the Risk-
===.2 Inservice Inspection===
Informed,
 
: [[ISI]] [[program that supersedes the]]
The inspector presented the inspection results 1R08 to Mr. Kevin Ostrowski, Director of Site Operations, and other members of the FENOC staff at the conclusion of the ISI inspection at an exit meeting on May 7, 2009. Some proprietary information was reviewed during this inspection and was either returned or properly destroyed, but no proprietary information is presented in this report.
ASME Section XI Code exam. The inspector
 
reviewed the manual UT examination data records of the "A" S/G cold and hot leg
===.3 Problem Identification and Resolution Submerged Cable Focus Sample===
nozzle-to-safe-end
 
: [[DM]] [[welds]]
The inspectors presented the inspection results Mr. Peter Sena, Beaver Valley Site Vice President, and other members of FENOC staff, at the conclusion of the inspection on June 11, 2009. No proprietary information is presented in this report.
RC-E-1A-N11 and RC-E-1A-N12.
 
b. Findings No findings of significance were identified. 4OA6 Meetings, Including Exit
===.4 Quarterly Exit Meeting Summary===
Enclosure .1 Access Control /
 
: [[ALA]] [[]]
On July 22, the inspectors presented the normal baseline inspection results to Mr. Ray Lieb, Director of Site Operations, and other members of the FENOC staff. The inspectors confirmed that proprietary information was not retained at the conclusion of the inspection period.  
RA Planning and Control The inspector presented the inspection results of 2S01 and 2S02 to Mr. Kevin Ostrowski,
{{a|4OA7}}
Director of Site Operations, and other members of
==4OA7 Licensee-Identified Violations==
: [[FEN]] [[]]
 
OC staff, at the conclusion of the
The following violation of very low safety significance (Green) was identified by the licensee and is a violation of NRC requirements which meets the criteria of Section VI of the NRC Enforcement Policy, NUREG-1600, for being dispositioned as an NCV.
inspection on April 30, 2009. No proprietary information is presented in this report.
* Technical Specification 3.6.1, "Containment," requires that containment operability be maintained in Mode 1, restored within one hour, or the reactor be shutdown to Mode 3 within six hours. Contrary to this requirement, FENOC failed  
.2 Inservice Inspection The inspector presented the inspection results 1R08 to Mr. Kevin Ostrowski, Director of
 
Site Operations, and other members of the
to maintain containment operability or restore cont ainment operability in the allowed time. Specifically, FENOC did not ensure containment isolation valves MOV-1RS-155B and MOV-1RS-156B were closed and de-energized prior to opening the 1RS-P-2B pump casing drain valve. The issue was entered into FENOC's corrective action program as CR 09-56250. The finding was more than minor because it is associated with the configuration control attribute of the barrier integrity cornerstone and affects the cornerstone objective of ensuring containment boundary preservation under postulated design-basis accident scenarios. The inspectors determined that the finding was of very low safety significance (Green), based on IMC 0609, Appendix H, Table 4.1 because this is a Type B finding and the affected pipe size is less than 2 inches in diameter.
: [[FENOC]] [[staff at the conclusion of the]]
 
ISI
ATTACHMENT:
inspection at an exit meeting on May 7, 2009. Some proprietary information was
 
reviewed during this inspection and was either returned or properly destroyed, but no
=SUPPLEMENTAL INFORMATION=
proprietary information is presented in this report.
 
.3 Problem Identification and Resolution Submerged Cable Focus Sample The inspectors presented the inspection results Mr. Peter Sena, Beaver Valley Site Vice
==KEY POINTS OF CONTACT==
President, and other members of
 
: [[FEN]] [[]]
===Licensee personnel===
OC staff, at the conclusion of the inspection on
 
June 11, 2009. No proprietary information is presented in this report.
G. Alberti  Steam Generator Program Owner  
.4 Quarterly Exit Meeting Summary On July 22, the inspectors presented the normal baseline inspection results to Mr. Ray
: [[contact::S. Baker  Site]], Radiation Protection Manager  
Lieb, Director of Site Operations, and other members of the
: [[contact::R. Bologna  Plant Engineering]], Manager
: [[FEN]] [[]]
T.Crella Senior Radiation Protection Technician  
OC staff. The
: [[contact::J. Fontaine  Supervisor]], ALARA
inspectors confirmed that proprietary information was not retained at the conclusion of
L. Freeland  Director Performance Improvement  
the inspection period. 4OA7 Licensee-Identified Violations The following violation of very low safety significance (Green) was identified by the
: [[contact::J. Freund  Supervisor]], Rad Operations Support  
licensee and is a violation of
: [[contact::D. Girdwood  Radiation Protection]], Quality Assessor
: [[NRC]] [[requirements which meets the criteria of Section]]
D. Grabski ISI Coordinator
VI of
T. Heimel NDE Level III  
the
: [[contact::W. Klinko]],  Diesel System Engineer
: [[NRC]] [[Enforcement Policy,]]
E. Lauck  System Engineer  
: [[NUREG]] [[-1600, for being dispositioned as an]]
: [[contact::R. Lubert  Electrical I&C/Plant Engineering]], Supervisor
: [[NCV.]] [[* Technical Specification 3.6.1, "Containment," requires that containment operability be maintained in Mode 1, restored within one hour, or the reactor be shutdown to Mode 3 within six hours. Contrary to this requirement,]]
FENOC failed
to maintain containment operability or restore containment operability in the allowed time. Specifically,
: [[FEN]] [[]]
: [[OC]] [[did not ensure containment isolation valves]]
: [[MOV]] [[-1]]
: [[RS]] [[-155B and]]
: [[MOV]] [[-1]]
RS-156B were closed and de-energized prior to
opening the
: [[1RS]] [[-P-2B pump casing drain valve. The issue was entered into]]
: [[FENOC]] [['s corrective action program as]]
CR 09-56250. The finding was more than
minor because it is associated with the configuration control attribute of the
barrier integrity cornerstone and affects the cornerstone objective of ensuring
containment boundary preservation under postulated design-basis accident
scenarios. The inspectors determined that the finding was of very low safety
significance (Green), based on IMC 0609, Appendix H, Table 4.1 because this is
a Type B finding and the affected pipe size is less than 2 inches in diameter.
: [[ATTACH]] [[]]
: [[MENT]] [[:]]
: [[SUPPLE]] [[]]
: [[MENTAL]] [[]]
: [[INFORM]] [[]]
: [[ATION]] [[Attachment]]
: [[SUPPLE]] [[]]
: [[MENTAL]] [[]]
: [[INFORM]] [[]]
: [[ATION]] [[]]
: [[KEY]] [[]]
: [[POINTS]] [[]]
: [[OF]] [[]]
CONTACT  Licensee personnel
G. Alberti  Steam Generator Program Owner
S. Baker  Site, Radiation Protection Manager
R. Bologna  Plant Engineering, Manager
: [[T.C]] [[rella Senior Radiation Protection Technician]]
: [[J.]] [[Fontaine  Supervisor,]]
ALARA
L. Freeland  Director Performance Improvement
J. Freund  Supervisor, Rad Operations Support
: [[D.]] [[Girdwood  Radiation Protection, Quality Assessor]]
: [[D.]] [[Grabski]]
: [[ISI]] [[Coordinator]]
: [[T.]] [[Heimel]]
NDE Level III
W. Klinko,  Diesel System Engineer
E. Lauck  System Engineer
R. Lubert  Electrical I&C/Plant Engineering, Supervisor
C. Miller  Senior Radiation Protection Technician
C. Miller  Senior Radiation Protection Technician
J. Miller  Site Fire Marshall
J. Miller  Site Fire Marshall  
B. Murtagh  Design, Supervisor
: [[contact::B. Murtagh  Design]], Supervisor  
: [[K.]] [[Ostrowski  Director, Site Operations]]
: [[contact::K. Ostrowski  Director]], Site Operations
: [[J.]] [[Patterson]]
J. Patterson RCS System Engineer
: [[RCS]] [[System Engineer]]
R. Pucci  Senior Nuclear Specialist - ALARA
: [[R.]] [[Pucci  Senior Nuclear Specialist -]]
P. Sena  Site Vice President  
ALARA
: [[contact::B. Sepelak  Supervisor]], Regulatory Compliance  
P. Sena  Site Vice President
: [[contact::D. Schwer  Manager]], Work Management
B. Sepelak  Supervisor, Regulatory Compliance
D. Schwer  Manager, Work Management
G. Storolis  Unit 2 Shift Manager
G. Storolis  Unit 2 Shift Manager
J. Tweddell  License Renewal  
J. Tweddell  License Renewal  


Other Personnel
Other Personnel
: [[D.]] [[Lew  Director, Division of Reactor Projects,]]
: [[contact::D. Lew  Director]], Division of Reactor Projects, NRC Region I  
: [[NRC]] [[Region I]]
: [[contact::R. Mathew  Team Leader]], NRC NRR  
: [[R.]] [[Mathew  Team Leader,]]
: [[contact::J. Rogge  Branch Chief]], NRC Region I
: [[NRC]] [[NRR]]
: [[contact::L. Ryan  Inspector]], Pennsylvania Department of Radiation Protection  
: [[J.]] [[Rogge  Branch Chief,]]
 
NRC Region I
==LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED==
: [[L.]] [[Ryan  Inspector, Pennsylvania Department of Radiation Protection]]
: [[LIST]] [[]]
: [[OF]] [[]]
: [[ITEMS]] [[]]
: [[OPENED]] [[,]]
: [[CLOSED]] [[,]]
: [[AND]] [[]]
: [[DISCUS]] [[]]
SED  Open/Closed
05000334 / 2009003-01 NCV Inadequate Post-Maintenance Testing Specified for Safety-Related River Water Check Valve. (Section 1R19)
05000334, 412 / 2009003-02
: [[NCV]] [[Continuously Submerged Cables Design Deficiency. (Section 4]]
OA2.3)
Attachment Closed
05000334 / 2009001-00 LER Surveillance test Inadvertently Violates Technical Specification 3.6.1 for Containment Operability. (Section
: [[4OA]] [[3.2)]]
: [[LIST]] [[]]
: [[OF]] [[]]
: [[DOCUME]] [[]]
: [[NTS]] [[]]
: [[REVIEW]] [[]]
ED  Section 1R01: Adverse Weather Protection
Procedures 1/2OM-53C.4A.35.1, Rev. 4, "Degraded Grid,"
: [[NOP]] [[-]]
: [[OP]] [[-1003, Rev. 0, "Grid Reliability Protocol,"]]
: [[NOP]] [[-]]
OP-1007, Rev. 5, "Risk Determination," 


Condition Reports 09-60033 09-60106
Open/Closed
: 05000334 / 2009003-01 NCV Inadequate Post-Maintenance Testing Specified for Safety-Related River Water Check Valve. (Section 1R19)
: 05000334, 412 / 2009003-02 NCV Continuously Submerged Cables Design Deficiency. (Section 4OA2.3)
Attachment
===Closed===
: 05000334 / 2009001-00 LER Surveillance test Inadvertently Violates Technical Specification 3.6.1 for Containment Operability. (Section
: 4OA3.2) 


Work Orders    200150639
==LIST OF DOCUMENTS REVIEWED==
200316056
==Section 1R01: Adverse Weather Protection==
200317926
200319210
200319961
200320671


Miscellaneous
===Procedures===
: [[BV]] [[-]]
: 1/2OM-53C.4A.35.1, Rev. 4, "Degraded Grid,"
PA-09-02, Summer Readiness PMS not Completed by June 1st
: NOP-OP-1003, Rev. 0, "Grid Reliability Pr otocol,"
Section 1R04:  Equipment Alignment
: NOP-OP-1007, Rev. 5, "Risk Determination,"
Procedures 1DBD-24, Design Basis Document for Feedwater System
===Condition Reports===
2OST-30.4, Service Water System A Header Valve Test
: 09-60033 09-60106 
2DBD-30, Design Basis Document for Service Water System
===Work Orders===
2OM-30.4.D, Spare Service Water Pump Startup
: 200150639
: 200316056
: 200317926
: 200319210
: 200319961
: 200320671 
===Miscellaneous===
: BV-PA-09-02, Summer Readiness PMS not Completed by June 1st


Drawings 10080-RM-0411-001, Rev. 15, "Valve Oper No. Diagram Low/High Head Safety Injection
==Section 1R04: Equipment Alignment==
08700-RM-0436-001, Rev. 11, "Valve Oper No. Diagram Emergency Diesel Generator Air Start System" 8700-RM-0436-002, Rev. 9, "Valve Oper No. Diagram Emergency Diesel Gen. Fuel Oil System"
10080-RM-430-1,
: [[VO]] [[]]
ND Service Water Supply & Distribution
10080-RM-430-2,
: [[VO]] [[]]
ND Service Water Primary Cooling
10080-RM-430-3,
: [[VO]] [[]]
ND Service Water Primary Cooling


Attachment Section 1R05Fire Protection  Procedures 1OST-33.21, Containment Penetrations Area Fire Protection Test
===Procedures===
: 1DBD-24, Design Basis Document for Feedwater System
: 2OST-30.4, Service Water System A Header Valve Test
: 2DBD-30, Design Basis Document for Service Water System
: 2OM-30.4.D, Spare Service Water Pump Startup  
===Drawings===
: 10080-RM-0411-001, Rev. 15, "Valve Oper No. Diagram Low/High Head Safety Injection
: 08700-RM-0436-001, Rev. 11, "Valve Oper No. Diagram Emergency Diesel Generator Air Start System" 8700-RM-0436-002, Rev. 9, "Valve Oper No. Diagram Emergency Diesel Gen. Fuel Oil System"
: 10080-RM-430-1, VOND Service Water Supply & Distribution
: 10080-RM-430-2, VOND Service Water Primary Cooling
: 10080-RM-430-3, VOND Service Water Primary Cooling
: Attachment


Condition Reports 02-11507 08-49244 09-57425* 09-57811 09-60284 09-60911
==Section 1R05: Fire Protection==
09-60761 09-60762


Miscellaneous Fire Protection Safe Shutdown Report; RTL# A1.080J, Addendum 28
===Procedures===
: [[RTL]] [[# A9.210X, Rev. 1]]
: 1OST-33.21, Containment Penetrations Area Fire Protection Test 
: [[BV]] [[]]
===Condition Reports===
: [[PS]] [[Unit 1 Appendix R Report, Chapter 11]]
: 2-11507 08-49244 09-57425* 09-57811 09-60284 09-60911
: [[BVPS]] [[Pre-Fire Plan for]]
: 09-60761 09-60762 
: [[ERF]] [[Substation and ERF diesel generator building]]
===Miscellaneous===
: [[BV]] [[]]
: Fire Protection Safe Shutdown Report; RTL# A1.080J, Addendum 28  
PS Event Logs, dated June 18, 2009
: RTL# A9.210X, Rev. 1  
Section 1R06:  Flood Protection  Documents reviewed are listed in section
: BVPS Unit 1 Appendix R Report, Chapter 11  
: [[4OA]] [[2 for this sample. Section 1R08:  Inservice Inspection  Procedures]]
: BVPS Pre-Fire Plan for ERF Substation and ERF diesel generator building  
: [[NDE]] [[-VT-513, Visual Examination of the Reactor Vessel Bottom Mounted Instrumentation (BMI) Nozzles, Rev.]]
: BVPS Event Logs, dated June 18, 2009
: [[3 NDE]] [[-]]
: [[UT]] [[-323, Ultrasonic Examination of Welds Joining Cast Austenitic Piping Components, Rev.]]
: [[2 ISIE]] [[-]]
ECP-2, Steam Generator Examination Program, Rev. 21
1&2
: [[ADM]] [[-2039,]]
BVPS ISI Ten-Year Plans, Rev. 8
1&2
: [[ADM]] [[-0801,]]
: [[ASME]] [[Section XI Repair/Replacement Program, Rev. 7]]
: [[NOP]] [[-]]
ER-2001, Boric Acid Corrosion Control Program, Rev. 7
Unit 1/2,
: [[NDE]] [[]]
: [[GP]] [[-105, Evaluation of]]
: [[PSI]] [[/]]
: [[ISI]] [[Flaw Indications, Rev. 9 Unit 1/2, ADM-2096, Alloy 600/690 Management Program, Rev. 7]]
: [[PWSCC]] [[Susceptibility Assessment of the Alloy 600 and Alloy 82/182 Components in Beaver Valley Units 1 and 2, dated December 2003]]
: [[NDE]] [[Examination Reports]]
: [[UT]] [[-09-1009, 2" socket welded]]
: [[RCS]] [[drain line RC-41-1502-Q1, completed 4/28/09]]
: [[UT]] [[-09-1062,]]
: [[RC]] [[-E-1A-N-11, Nozzle to safe-end DM weld (Hot Leg), completed 5/6/09]]
: [[UT]] [[-09-1063,]]
: [[RC]] [[-E-1A-N-12, Nozzle to safe-end DM weld (Cold Leg), completed 5/6/09]]
: [[PT]] [[-09-1003,]]
: [[RH]] [[-1-1-A-01 to 02, Welded attachment support SH-40, completed 4/29/09]]
: [[PT]] [[-09-1004,]]
: [[RH]] [[-1-1-A-01 to 02, Welded attachment support SH-40, completed 5/01/09]]
: [[UT]] [[-09-1055,]]
: [[DLW]] [[-LOOP3-7-S-02, RCS "C" loop cold leg pipe girth weld, completed 5/5/09]]
: [[UT]] [[-09-1039, 1]]
: [[CNMT]] [[-Liner Area #3, completed 5/1/09]]
: [[BOP]] [[-]]
: [[MT]] [[-09-029,]]
: [[BV]] [[-1-]]
: [[RCBX]] [[, Primary Containment, Liner repair root pass, completed 5/4/09]]
: [[BOP]] [[-]]
: [[MT]] [[-09-031,]]
: [[BV]] [[-1-]]
: [[RCBX]] [[, Primary Containment, Liner plate final, completed 5/4/09]]
: [[BOP]] [[-]]
: [[MT]] [[-09-032,]]
: [[BV]] [[-1-]]
: [[RCBX]] [[, Primary Containment, Liner plate final, completed 5/4/09]]
: [[BOP]] [[-]]
: [[UT]] [[-09-161, Containment liner repair plate butt weld, 45-degree scan, completed 5/4/09]]
: [[BOP]] [[-]]
: [[UT]] [[-09-162, Containment liner repair plate butt weld, 60-degree scan, completed 5/4/09]]
: [[BOP]] [[-]]
: [[VT]] [[-09-042,]]
: [[VT]] [[-1,]]
: [[RBC]] [[Liner plate weld, completed 5/4/09]]
: [[SG]] [[-]]
CDME-07-24, BV Unit 1 Steam Generator Degradation Assessment 1R18 Refueling Outage, Rev.1
Attachment Work Orders 200367661 200366975 200367239 200367242


Condition Reports 07-25709 09-52089 09-54434 09-57589 09-57762 09-57665
==Section 1R06: Flood Protection==
09-57804 09-58004 09-58156
Section 1R12: Maintenance Rule Implementation  Procedures 1OST-15.1, Reactor Plant Component Cooling Water Pump Operating Surveillance Test  Condition Reports 07-27037 09-60127 09-59359
Section 1R13:  Maintenance Risk Assessment and Emergent Work Control  Calculations 8700-DMC-1669, Rev. 1, Add. 1, "Time to RCS Boiling Calculation for the Pre-outage Shutdown Defense-in-Depth Report."


Procedures
===Documents===
: [[NOP]] [[-]]
reviewed are listed in section 4OA2 for this sample.
OP-1007, Rev. 5, "Risk Determination"
1/2-ADM-2033, "Risk Management Program"


Work Orders
==Section 1R08: Inservice Inspection==
Condition Reports 09-57463 09-58491 09-58771 09-58775 09-58815


Other 1R19 Defense-In-Depth review for April 21, 2009
===Procedures===
Unit 1 Weekly Maintenance Risk Summary for the week of June 15, Revs. 0 & 2
: NDE-VT-513, Visual Examination of the Reactor Vessel Bottom Mounted Instrumentation (BMI) Nozzles, Rev. 3
Unit 2 Weekly Maintenance Risk Summary for the week of June 15, Revs. 0 & 2
: NDE-UT-323, Ultrasonic Examination of Welds Joining Cast Austenitic Piping Components, Rev. 2
Section 1R15: Operability Evaluations  Calculations 8700-UR(B)-511
: ISIE-ECP-2, Steam Generator Examination Program, Rev. 21
10080-UR(B)-510
: 1&2
241-UR(B)-427  Procedures 1OST-24.15B "Auxiliary Feedwater System Solid State Protection System Testing Train B"
: ADM-2039, BVPS ISI Ten-Year Plans, Rev. 8
Condition Reports 04-05251
: 1&2
06-01122
: ADM-0801, ASME Section XI Repair/Replacement Program, Rev. 7
09-57966
: NOP-ER-2001, Boric Acid Corrosion Control Program, Rev. 7
09-58000
: Unit 1/2, NDE
09-58798
: GP-105, Evaluation of PSI/ISI Flaw Indications, Rev. 9 Unit 1/2,
09-59713
: ADM-2096, Alloy 600/690 Management Program, Rev. 7
Attachment Miscellaneous Event Notification 45015, dated April 23, 2009
: PWSCC Susceptibility Assessment of the Alloy 600 and Alloy 82/182 Components in Beaver Valley Units 1 and 2, dated December 2003
Engineering Change 09-0365-01, Repair Containment Liner Plate Hole
: NDE Examination Reports
IN 2005-24
: UT-09-1009, 2" socket welded RCS drain line
L-09-119,
: RC-41-1502-Q1, completed 4/28/09
: [[10CFR]] [[50.55a Request Number]]
: UT-09-1062,
BV1-IWE-2-2, dated April 28, 2009
: RC-E-1A-N-11, Nozzle to safe-end DM weld (Hot Leg), completed 5/6/09
Mode Hold Resolutions for 09-57589, 09-57762
: UT-09-1063,
: [[NO]] [[]]
: RC-E-1A-N-12, Nozzle to safe-end DM weld (Cold Leg), completed 5/6/09
: [[TF]] [[600538028, 600538316]]
: PT-09-1003,
: [[NUR]] [[]]
: RH-1-1-A-01 to 02, Welded attachment support
EG-1522, Assessment of Inservice Conditions of Safety-Related Nuclear Plant Structures
: SH-40, completed 4/29/09
RIS 2009-02, Rev. 1, "Use of Containment Atmosphere Gaseous Radioactivity Monitors for
: PT-09-1004,
Reactor Coolant System Leakage Detection Equipment at Nuclear Power Reactors"
: RH-1-1-A-01 to 02, Welded attachment support
: [[TS]] [[]]
: SH-40, completed 5/01/09
TF-513
: UT-09-1055,
WO 200124471, 200367013, 200367242
: DLW-LOOP3-7-S-02, RCS "C" loop cold leg pipe girth weld, completed 5/5/09
Unit 2 Fire Protection Safe Shutdown Report
: UT-09-1039, 1CNMT-Liner Area #3, completed 5/1/09
Section 1R18Plant Modifications
: BOP-MT-09-029,
Condition Reports 09-57390
: BV-1-RCBX, Primary Containment, Liner repair root pass, completed 5/4/09
: BOP-MT-09-031,
: BV-1-RCBX, Primary Containment, Liner plate final, completed 5/4/09
: BOP-MT-09-032,
: BV-1-RCBX, Primary Containment, Liner plate final, completed 5/4/09
: BOP-UT-09-161, Containment liner repair plate butt weld, 45-degree scan, completed 5/4/09
: BOP-UT-09-162, Containment liner repair plate butt weld, 60-degree scan, completed 5/4/09
: BOP-VT-09-042,
: VT-1, RBC Liner plate weld, completed 5/4/09
: SG-CDME-07-24, BV Unit 1 Steam Generator Degradation Assessment 1R18 Refueling Outage, Rev.1
: Attachment Work Orders
: 200367661
: 200366975
: 200367239
: 200367242
===Condition Reports===
: 07-25709 09-52089 09-54434 09-57589 09-57762 09-57665  
: 09-57804 09-58004 09-58156


Regulatory Applicability Determination and 10 CFR 50.59 Screens 09-01453 09-0174 
==Section 1R12: Maintenance Rule Implementation==


Procedures 1OM-52.4.R.1.F, Station Shutdown from 100% Power to Mode 5.
===Procedures===
: 1OST-15.1, Reactor Plant Component Cooling Water Pump Operating Surveillance Test 
===Condition Reports===
: 07-27037 09-60127 09-59359


Drawings 8700-6.24-158 sheet1, Rev. 7
==Section 1R13: Maintenance Risk Assessment and Emergent Work Control==
8700-6.24-158 sheet 8, Rev. 2
8700-6.24-158, sheet 9, Rev. 2
8700-RM-0430-001, Rev 30
8700-RM-407-1, Rev. 28
8700-2.19-0036, Rev. A


Work Orders 200359549 200359555 200313752 200313753
===Calculations===
: 8700-DMC-1669, Rev. 1, Add. 1, "Time to RCS Boiling Calculation for the Pre-outage Shutdown Defense-in-Depth Report." 
===Procedures===
: NOP-OP-1007, Rev. 5, "Risk Determination"
: 1/2-ADM-2033, "Risk Management Program" 
===Work Orders===


Miscellaneous
===Condition Reports===
: [[NUREG]] [[-0138,]]
: 09-57463 09-58491 09-58771 09-58775 09-58815
: [[NUREG]] [[-0224]]
: Other 1R19 Defense-In-Depth review for April 21, 2009
: [[EGG]] [[-]]
: Unit 1 Weekly Maintenance Risk Summary for the week of June 15, Revs. 0 & 2  
EA-5826, TER Evaluation Report of the Overpressure protection System for the Beaver
: Unit 2 Weekly Maintenance Risk Summary for the week of June 15, Revs. 0 & 2
Valley Power Station Unit 1, dated March 1982.
Section 1R19:  Post-Maintenance Testing
Procedures
: [[1OST]] [[-36.2, Rev. 51, "Diesel Generator No. 2 Monthly Test"]]
: [[1OM]] [[-36.4]]
AN, Rev. 2, "Diesel Generator No. 2 Fast Start"


Work Orders 200124471 200308605 200284373 200296714 200296713
==Section 1R15: Operability Evaluations==
200367242 200369010 200233562


Attachment Condition Reports 09-57435 09-57813 09-58940
===Calculations===
: 8700-UR(B)-511
: 10080-UR(B)-510
: 241-UR(B)-427 
===Procedures===
: 1OST-24.15B "Auxiliary Feedwater System Solid State Protection System Testing Train B" 
===Condition Reports===
: 04-05251
: 06-01122
: 09-57966
: 09-58000
: 09-58798
: 09-59713 
: Attachment Miscellaneous Event Notification 45015, dated April 23, 2009
: Engineering Change 09-0365-01, Repair Containment Liner Plate Hole
: IN 2005-24
: L-09-119, 10CFR 50.55a Request Number
: BV1-IWE-2-2, dated April 28, 2009
: Mode Hold Resolutions for 09-57589, 09-57762
: NOTF
: 600538028,
: 600538316
: NUREG-1522, Assessment of Inservice Conditions of Safety-Related Nuclear Plant Structures
: RIS 2009-02, Rev. 1, "Use of Containment Atmosphere Gaseous Radioactivity Monitors for Reactor Coolant System Leakage Detection Equipment at Nuclear Power Reactors"
: TSTF-513
: WO 200124471,
: 200367013,
: 200367242
: Unit 2 Fire Protection Safe Shutdown Report


Miscellanous  Section 1R20: Refueling and Outage Activities
==Section 1R18: Plant Modifications==
Procedures
: [[1BVT]] [[-1.1.1, Rev. 4, "Rod Position Indication System Calibration Verification and Control Rod  Drop Test" 1]]
: [[BVT]] [[2.1.1, Issue 1, Rev. 0, "Control Rod plant Exercise and Data Collection"]]
: [[1OM]] [[-6.4.]]
AO, Rev. 20, "Isolating and Draining a Reactor Coolant Loop"
1OM-20.4E, Rev. 31, "Draining The Refueling Cavity"
1OM-50.4D, Rev. 49, "Reactor Startup From Mode 3 to Mode 2"
: [[1OM]] [[-50.4L, Rev. 18, "Plant Heatup From Mode 6 to Mode 3"]]
: [[1OM]] [[-50.4L, Rev. 18, "Plant Heatup From Mode 6 to Mode 3, Data Sheet 2:]]
: [[RCS]] [[Heatup / Cooldown Determination" 1OM-52.4.K, Rev. 0, "Tavg Coastdown Operations"]]
: [[1OM]] [[-52.4.R.1.F, Rev. 14, "Station Shutdown from 100% Power to Mode 5", Data Sheet 2:]]
RCS Cooldown Determination Tables. 1OST-47.2B, Rev. 7, "Containment Closeout Inspection"
1OST-49.2, Rev. 22, "Shutdown Margin Calculation (Plant Shutdown) (Updated for Cycle 19)"
1MSP-9.04-M, Rev. 8, "Containment Sump Inspection"
1RP-3.2, Issue 0, Rev. 3, "Fuel Transfer System"
1RP-3.26, Rev. 7, "Refueling Procedure Upper Internals Assembly Installation"
1RP-3.28, Rev. 4, "Lower Internals Assembly Removal / Installation"
1RST-2.1, Rev. 11, "Initial Approach to Criticality After Refueling"
: [[1RST]] [[-2.2, Rev. 10, "Core Design Check Test"]]
: [[NOBP]] [[-]]
: [[OM]] [[-4010, Rev. 4, "Restart Readiness for Plant Outages"]]
: [[NOBP]] [[-]]
: [[WM]] [[-5003, Rev. 1, "FENOC Rigging and Lifting Manual"]]
: [[NOP]] [[-]]
: [[OP]] [[-1005, Rev. 10, "Shutdown Defense in Depth"]]
: [[NOP]] [[-]]
WM-5003, Rev. 1, "Rigging, Lifting, and Load Handling"


Drawings 8700-02.102-0050, Rev. A, "General Arrangement Transfer System"
===Condition Reports===
Cable Drive Installation, Transfer System -
: 09-57390
: [[BV]] [[]]
: Regulatory Applicability Determination and 10
PS1, Rev. 1  
: CFR 50.59 Screens
: 09-01453 09-0174
===Procedures===
: 1OM-52.4.R.1.F, Station Shutdown from 100% Power to Mode 5.
===Drawings===
: 8700-6.24-158 sheet1, Rev. 7
: 8700-6.24-158 sheet 8, Rev. 2
: 8700-6.24-158, sheet 9, Rev. 2
: 8700-RM-0430-001, Rev 30
: 8700-RM-407-1, Rev. 28
: 8700-2.19-0036, Rev.
===Work Orders===
: 200359549
: 200359555
: 200313752
: 200313753 
===Miscellaneous===
: NUREG-0138,
: NUREG-0224
: EGG-EA-5826, TER Evaluation Report of the Overpressure protection System for the Beaver Valley Power Station Unit 1, dated March 1982.


Work Orders Repetitive Task 10001 99-0201123-000 200285260 600426477
==Section 1R19: Post-Maintenance Testing==


Miscellaneous 1R19 Outage Handbook
===Procedures===
Defense-In-Depth Report, 1R19, dated April 6, 2009 and updated May 16, 2009
: 1OST-36.2, Rev. 51, "Diesel Generator No. 2 Monthly Test"
Operating Experience Handbook for
: 1OM-36.4AN, Rev. 2, "Diesel Generator No. 2 Fast Start" 
: [[BV]] [[1R19]]
===Work Orders===
: [[ECP]] [[09-0035-001,]]
: 200124471
BV1 and BV2 Tave / Power Coastdown, Master Package
: 200308605
8700-02.102-0010,
: 200284373
: [[UE&C]] [[Instruction Manual Cable Drive Fuel Transfer System]]
: 200296714
: [[BV]] [[]]
: 200296713
PS-1 Shift Operating / Refueling Logs dated April 19 - May 22, 2009
: 200367242
: [[BV]] [[Unit 1 Cycle 20 Loading Pattern Map and Verification Video, reviewed May 12, 2009]]
: 200369010
: [[NUR]] [[]]
: 200233562
EG-0612
: Attachment Condition Reports
Primavera Schedule, 1R19
: 09-57435 09-57813 09-58940
: Miscellanous


Attachment Condition Reports 09-57474
==Section 1R20: Refueling and Outage Activities==
09-57499
09-57762
09-57106
09-57589
09-59677
09-59702
09-60367
09-60572
Section 1R22: Surveillance Testing  Procedures
: [[1OST]] [[-36.3, Train A]]
: [[EDG]] [[Autoload Test]]
: [[1BVT]] [[-2.15.1, Rev. 5, " Reactor Plant Component Cooling Water Pumps [1]]
CC-P-1A], [1CC-P-1B], [1CC-P-1C] Performance Curve Development"
Condition Reports 09-56250 09-57623 09-60127


Work Orders & Notifications
===Procedures===
: [[WO]] [[200309388]]
: 1BVT-1.1.1, Rev. 4, "Rod Position Indication System Calibration Verification and Control Rod
: [[NO]] [[]]
: Drop Test" 1BVT 2.1.1, Issue 1, Rev. 0, "Control Rod plant Exercise and Data Collection" 
TF 600537878
: 1OM-6.4.AO, Rev. 20, "Isolating and Draining a Reactor Coolant Loop"
: 1OM-20.4E, Rev. 31, "Draining The Refueling Cavity" 
: 1OM-50.4D, Rev. 49, "Reactor Startup From Mode 3 to Mode 2"
: 1OM-50.4L, Rev. 18, "Plant Heatup From Mode 6 to Mode 3" 
: 1OM-50.4L, Rev. 18, "Plant Heatup From Mode 6 to Mode 3, Data Sheet 2: RCS Heatup / Cooldown Determination" 1OM-52.4.K, Rev. 0, "Tavg Coastdown Operations"
: 1OM-52.4.R.1.F, Rev. 14, "Station Shutdown from 100% Power to Mode 5", Data Sheet 2: RCS Cooldown Determination Tables. 1OST-47.2B, Rev. 7, "Containment Closeout Inspection"
: 1OST-49.2, Rev. 22, "Shutdown Margin Calculation (Plant Shutdown) (Updated for Cycle 19)"
: 1MSP-9.04-M, Rev. 8, "Containment Sump Inspection"
: 1RP-3.2, Issue 0, Rev. 3, "Fuel Transfer System"
: 1RP-3.26, Rev. 7, "Refueling Procedure Upper Internals Assembly Installation"
: 1RP-3.28, Rev. 4, "Lower Internals Assembly Removal / Installation"
: 1RST-2.1, Rev. 11, "Initial Approach to Criticality After Refueling"
: 1RST-2.2, Rev. 10, "Core Design Check Test"
: NOBP-OM-4010, Rev. 4, "Restart Readiness for Plant Outages"
: NOBP-WM-5003, Rev. 1, "FENOC Rigging and Lifting Manual"
: NOP-OP-1005, Rev. 10, "Shutdown Defense in Depth"
: NOP-WM-5003, Rev. 1, "Rigging, Lifting, and Load Handling" 
===Drawings===
: 8700-02.102-0050, Rev. A, "General Arrangement Transfer System" Cable Drive Installation, Transfer System - BVPS1, Rev. 1 
===Work Orders===
: Repetitive Task 10001 99-0201123-000
: 200285260
: 600426477 
===Miscellaneous===
: 1R19 Outage Handbook Defense-In-Depth Report, 1R19, dated April 6, 2009 and updated May 16, 2009 
===Operating Experience===
: Handbook for BV 1R19
: ECP 09-0035-001, BV1 and BV2 Tave / Power Coastdown, Master Package
: 8700-02.102-0010, UE&C Instruction Manual Cable Drive Fuel Transfer System
: BVPS-1 Shift Operating / Refueling Logs dated April 19 - May 22, 2009
: BV Unit 1 Cycle 20 Loading Pattern Map and Verification Video, reviewed May 12, 2009
: NUREG-0612
: Primavera Schedule, 1R19
: Attachment Condition Reports
: 09-57474
: 09-57499
: 09-57762
: 09-57106
: 09-57589
: 09-59677
: 09-59702
: 09-60367
: 09-60572


Miscellaneous Unit 1 Shift Operating Logs dated March 26 - 28, 2009
==Section 1R22: Surveillance Testing==
Sections
: [[2OS]] [[1Access Control to Radiologically Significant Areas and  2]]
: [[OS]] [[2]]
: [[ALA]] [[]]
RA Planning and Controls
Procedures 1/2-ADM-1601, Rev 15, Radiation Protection Standards
1/2-ADM-1611, Rev 9, Radiation Protection Administrative Guide
1/2-ADM-1621, Rev 3,
: [[ALA]] [[]]
RA Program
1/2-ADM-1630, Rev 10, Radiation Worker Practices
1/2-ADM-1631, Rev 5, Exposure Control
1/2-HPP-3.02.004, Rev 4, Area Posting
1/2-HPP-3.03.007, Rev 3, Transfer of Highly Radioactive Material from Plant Systems to Solid Waste 1/2-HPP-3.04.002, Rev 5, Bioassay Administration
1/2-HPP-3.05.001, Rev 4, Exposure Authorization
1/2-HPP-3.07.002, Rev 5, Radiation Survey Methods
1/2-HPP-3.07.013, Rev 3, Barrier Checks
1/2-HPP-3.08.001, Rev 8, Radiological Work Permit
1/2-HPP-3.08.003, Rev 10, Radiation Barrier Key Control
1/2-HPP-3.08.005, Rev 4,
: [[ALA]] [[]]
RA Review Program
1/2-HPP-3.08.006, Rev 1, Shielding
: [[BVBP]] [[-]]
: [[RP]] [[-0003, Rev 4, Dosimetry Practices]]
: [[BVBP]] [[-]]
RP-0013, Rev 2, Radiation Protection Risk Assessment Process
Attachment
: [[BVBP]] [[-]]
: [[RP]] [[-0020, Rev 6,]]
: [[RP]] [[Job Coverage General Guidance]]
: [[NOP]] [[-WM-7001, Rev 0,]]
: [[ALA]] [[]]
: [[RA]] [[Program]]
: [[NOP]] [[-]]
: [[WM]] [[-7002, Rev 0, Operational]]
: [[ALA]] [[]]
: [[RA]] [[Program]]
: [[NOP]] [[-]]
: [[WM]] [[-7003, Rev 0, Radiation Work Permit]]
: [[NOP]] [[-]]
: [[WM]] [[-7017, Rev 0, Contamination Control Program]]
: [[NOP]] [[-]]
WM-7021, Rev 1, Radiological Postings, Labeling, and Markings
1/2-OM-18.4A.E, Rev 6, Removal of Spent Filter Cartridge From Filter Transfer Cask  Nuclear Oversight Field Observation Reports Week of 4/20-26/2009  Condition Reports 09-58093 09-58195 09-58182 09-58115 09-58029 09-58162
09-58104 09-58043 09-58042 09-57896 09-57877 09-57843
09-57918 09-57701 09-57747 09-57797 09-57790 09-57810
09-57914 09-57901 09-55024 09-56516 09-56588 09-57570
09-57882
: [[ALA]] [[]]
RA Plans & related Work-in-Progress /Post-Job Reviews 09-01-35, Permanent Scaffolding
09-01-33, Insulation Modifications (except Cavity Work)
09-01-25, Reactor Disassembly
09-01-41, Routine Valve Work
09-01-19, Replace/Dispose of Incore Detectors
09-01-24, Secondary Side Steam Generator Sludge Lancing/FOSAR
09-01-58, Flush/Change Resin
09-01-11, Changeout/Replace
: [[1CH]] [[-]]
FL-2 Filter
09-01-33, Insulation Removal/Replacement Modification
09-01-26, Remove/Replace Incore Detectors
09-01-29, In-Service Inspections
09-01-31, Scaffolding
: [[ALA]] [[]]
RA Committee Meeting Minutes Meeting Nos. 09-01m/s, 09-02 m/s, 09-03 m/s, 09-04m/s, 09-05 m/s, 09-06 m, 09-07 m,
09-08 m, 09-09 m (m-manager's, s-subcommittee)  Miscellaneous
: [[ALARA]] [[Reports 1R19 Outage]]
: [[ALARA]] [[Plan]]
: [[EP]] [[]]
RI Standard Radiation Monitoring Program - Unit 1 Source Term Measurements
High Dose Individuals for 2009
Dose and Dose Rate Alarm Reports for 2009  Section
: [[4OA]] [[2:  Problem Identification and Resolution  Procedures]]
NORM-ER-3112, Rev. 1, Cable Monitoring
1/2-PMP-E-75-001, 4160 Rev. 8, VAC Motor Inspection and Lubrication
1/2-75-MANHOLE-1E, Rev. 4, Inspection of Manholes for Water Induced Damage  Completed Procedures 1/2-PMP-E-75-001, 4160 VAC Motor Inspection and Lubrication, Rev. 8 dated 12/27/07
1/2-PMP-E-75-001, 4160 VAC Motor Inspection and Lubrication, Rev. 8 dated 02/08/08
Attachment 1/2-PMP-E-75-001,
: [[4160 VAC]] [[Motor Inspection and Lubrication, Rev. 8 dated 08/15/08 1/2-]]
PMP-E-75-001, 4160 VAC Motor Inspection and Lubrication, Rev. 8 dated 07/01/08
1/2-PMP-E-75-001, 4160 VAC Motor Inspection and Lubrication, Rev. 8 dated 05/19/08
1/2-PMP-E-75-001, 4160 VAC Motor Inspection and Lubrication, Rev. 8 dated 02/24/08
1/2-75-MANHOLE-1E, Inspection of Manholes for Water Induced Damage, Rev. 4 dated 09/26/06 1/2-75-MANHOLE-1E, Inspection of Manholes for Water Induced Damage, Rev. 4 dated 11/07/08
Miscellaneous:
: [[BV]] [[]]
UFSAR Unit 1, Rev. 20
Kerite Letter dated December 5, 1991
Kerite Letter dated February 18, 2009
: [[GL]] [[2007-01, Inaccessible of Underground Power Cable Failures That Disable Accident Mitigation Systems or Cause Plant Transients]]
: [[IN]] [[2002-12, Submerged Safety-Related Electrical Cables]]
: [[IEEE]] [[400.2,]]
IEEE Guide for Field Testing of Shielded Power Cable Systems Using Very Low Frequency (VLF) Westinghouse Issue Report 08-124-M001


Condition Reports: 02-02302
===Procedures===
2-02348
: 1OST-36.3, Train A EDG Autoload Test
06-04144
: 1BVT-2.15.1, Rev. 5, " Reactor Plant Component Cooling Water Pumps [1CC-P-1A], [1CC-P-1B], [1CC-P-1C] Performance Curve Development" 
06-06305
===Condition Reports===
08-39693
: 09-56250 09-57623 09-60127 
08-42380
===Work Orders===
08-43594
& Notifications
09-60316
: WO 200309388
09-60387
: NOTF
Section 4OA3Event Response
: 600537878 
Condition Reports 09-57474
===Miscellaneous===
09-58477
: Unit 1 Shift Operating Logs dated March 26 - 28, 2009
09-58873
: Sections 2OS1Access Control to Radiologically Significant Areas and
09-58900
: 2OS2 ALARA Planning and Controls
09-58905
===Procedures===
09-59155
: 1/2-ADM-1601, Rev 15, Radiation Protection Standards
09-60763
: 1/2-ADM-1611, Rev 9, Radiation Protection Administrative Guide
09-60768
: 1/2-ADM-1621, Rev 3, ALARA Program
: 1/2-ADM-1630, Rev 10, Radiation Worker Practices
: 1/2-ADM-1631, Rev 5, Exposure Control
: 1/2-HPP-3.02.004, Rev 4, Area Posting
: 1/2-HPP-3.03.007, Rev 3, Transfer of Highly Radioactive Material from Plant Systems to Solid Waste 1/2-HPP-3.04.002, Rev 5, Bioassay Administration
: 1/2-HPP-3.05.001, Rev 4, Exposure Authorization
: 1/2-HPP-3.07.002, Rev 5, Radiation Survey Methods
: 1/2-HPP-3.07.013, Rev 3, Barrier Checks
: 1/2-HPP-3.08.001, Rev 8, Radiological Work Permit
: 1/2-HPP-3.08.003, Rev 10, Radiation Barrier Key Control
: 1/2-HPP-3.08.005, Rev 4, ALARA Review Program
: 1/2-HPP-3.08.006, Rev 1, Shielding
: BVBP-RP-0003, Rev 4, Dosimetry Practices
: BVBP-RP-0013, Rev 2, Radiation Protection Risk Assessment Process Attachment
: BVBP-RP-0020, Rev 6, RP Job Coverage General Guidance
: NOP-WM-7001, Rev 0, ALARA Program
: NOP-WM-7002, Rev 0, Operational ALARA Program
: NOP-WM-7003, Rev 0, Radiation Work Permit
: NOP-WM-7017, Rev 0, Contamination Control Program
: NOP-WM-7021, Rev 1, Radiological Postings, Labeling, and Markings
: 1/2-OM-18.4A.E, Rev 6, Removal of Spent Filter Cartridge From Filter Transfer Cask Nuclear Oversight Field Observation Reports Week of 4/20-26/2009 
===Condition Reports===
: 09-58093 09-58195 09-58182 09-58115 09-58029 09-58162
: 09-58104 09-58043 09-58042 09-57896 09-57877 09-57843
: 09-57918 09-57701 09-57747 09-57797 09-57790 09-57810
: 09-57914 09-57901 09-55024 09-56516 09-56588 09-57570
: 09-57882
: ALARA Plans & related Work-in-Progress /Post-Job Reviews
: 09-01-35, Permanent Scaffolding
: 09-01-33, Insulation Modifications (except Cavity Work)
: 09-01-25, Reactor Disassembly  
: 09-01-41, Routine Valve Work
: 09-01-19, Replace/Dispose of Incore Detectors
: 09-01-24, Secondary Side Steam Generator Sludge Lancing/FOSAR
: 09-01-58, Flush/Change Resin
: 09-01-11, Changeout/Replace 1CH-FL-2 Filter
: 09-01-33, Insulation Removal/Replacement Modification
: 09-01-26, Remove/Replace Incore Detectors
: 09-01-29, In-Service Inspections
: 09-01-31, Scaffolding
: ALARA Committee Meeting Minutes Meeting Nos. 09-01m/s, 09-02 m/s, 09-03 m/s, 09-04m/s, 09-05 m/s, 09-06 m, 09-07 m, 
: 09-08 m, 09-09 m (m-manager's, s-subcommittee)
===Miscellaneous===
: ALARA Reports
: 1R19 Outage ALARA Plan 
: EPRI Standard Radiation Monitoring Program - Unit 1 Source Term Measurements High Dose Individuals for 2009
: Dose and Dose Rate Alarm Reports for 2009


Procedures 1/2-EPP-IP-1.1, Rev. 43, "Notifications", Att B. Unusual Event - Control Room
==Section 4OA2: Problem Identification and Resolution==
1/2-EPP-IP-1.2, Rev. 35, "Unusual Event"
1/2-EPP-IP-1.1.F01, Nuclear Power Plant Initial Notification Form, dated June 18, 2009
: [[1OM]] [[-1.4.Z, Rev.0, "]]
ESF Signal Reset By Alternate Method"


Attachment Work Orders 200366604
===Procedures===
200306521
: NORM-ER-3112, Rev. 1, Cable Monitoring
200366962
: 1/2-PMP-E-75-001, 4160 Rev. 8, VAC Motor Inspection and Lubrication
200366752
: 1/2-75-MANHOLE-1E, Rev. 4, Inspection of Manholes for Water Induced Damage Completed Procedures
200351634
: 1/2-PMP-E-75-001, 4160 VAC Motor Inspection and Lubrication, Rev. 8 dated 12/27/07
200306527
: 1/2-PMP-E-75-001, 4160 VAC Motor Inspection and Lubrication, Rev. 8 dated 02/08/08 
200390431
: Attachment 1/2-PMP-E-75-001, 4160 VAC Motor Inspection and Lubrication, Rev. 8 dated 08/15/08 1/2-PMP-E-75-001, 4160 VAC Motor Inspection and Lubrication, Rev. 8 dated 07/01/08
: 1/2-PMP-E-75-001, 4160 VAC Motor Inspection and Lubrication, Rev. 8 dated 05/19/08
: 1/2-PMP-E-75-001, 4160 VAC Motor Inspection and Lubrication, Rev. 8 dated 02/24/08
: 1/2-75-MANHOLE-1E, Inspection of Manholes for Water Induced Damage, Rev. 4 dated 09/26/06 1/2-75-MANHOLE-1E, Inspection of Manholes for Water Induced Damage, Rev. 4 dated 11/07/08 
: Miscellaneous:
: BV UFSAR Unit 1, Rev. 20
: Kerite Letter dated December 5, 1991
: Kerite Letter dated February 18, 2009
: GL 2007-01, Inaccessible of Underground Power Cable Failures That Disable Accident Mitigation Systems or Cause Plant Transients
: IN 2002-12, Submerged Safety-Related Electrical Cables
: IEEE 400.2, IEEE Guide for Field Testing of Shielded Power Cable Systems Using Very Low Frequency (VLF) Westinghouse Issue Report 08-124-M001
: Condition Reports:
: 2-02302
: 2-02348
: 06-04144
: 06-06305
: 08-39693
: 08-42380
: 08-43594
: 09-60316
: 09-60387


Event Notifications 45000, dated April 20, 2009
==Section 4OA3: Event Response==
45001, dated April 20, 2009
45001 (retraction), dated May 12, 2009
45015, dated April 23, 2009
45022, dated April 26, 2009
45099, dated May 28, 2009
45143, dated June 18, 2009


Miscellaneous:
===Condition Reports===
: [[BV]] [[-]]
: 09-57474
: [[SA]] [[-09-018, Snapshot Self-Assessment for Unit 1 Inadvertent]]
: 09-58477
: [[SSPS]] [[Train A]]
: 09-58873
: [[SI]] [[Signal on May 6, 2009 Mode Hold Resolutions for CRs 09-57499, 09-57474, 09-57762, 09-57589, 09-58004]]
: 09-58900
: [[NRC]] [[Op]]
: 09-58905
ESS 2009-02, "Negative Trend and Recurring Events Involving Feedwater Systems"
: 09-59155
Shift Logs dated, June 18, 2009
: 09-60763
Event Timeline, June 18, 2009
: 09-60768 
: [[LIST]] [[]]
===Procedures===
: [[OF]] [[]]
: 1/2-EPP-IP-1.1, Rev. 43, "Notifications", Att B. Unusual Event - Control Room
: [[ACRONY]] [[]]
: 1/2-EPP-IP-1.2, Rev. 35, "Unusual Event"
: [[MS]] [[ADM  Administrative Procedure]]
: 1/2-EPP-IP-1.1.F01, Nuclear Power Plant Initial Notification Form, dated June 18, 2009
: [[ALA]] [[]]
: 1OM-1.4.Z, Rev.0, "ESF Signal Reset By Alternate Method"
: [[RA]] [[As Low As is Reasonably Achievable]]
: Attachment Work Orders
: 200366604
: 200306521
: 200366962
: 200366752
: 200351634
: 200306527
: 200390431
: Event Notifications
: 45000, dated April 20, 2009
: 45001, dated April 20, 2009
: 45001 (retraction), dated May 12, 2009
: 45015, dated April 23, 2009
: 45022, dated April 26, 2009
: 45099, dated May 28, 2009
: 45143, dated June 18, 2009
: Miscellaneous:
: BV-SA-09-018, Snapshot Self-Assessment for Unit 1 Inadvertent SSPS Train A SI Signal on May 6, 2009 Mode Hold Resolutions for CRs 09-57499, 09-57474, 09-57762, 09-57589, 09-58004  
: NRC OpESS 2009-02, "Negative Trend and Recurring Events Involving Feedwater Systems" Shift Logs dated, June 18, 2009  
: Event Timeline, June 18, 2009
==LIST OF ACRONYMS==
: [[ADM]] [[Administrative Procedure]]
: [[ALARA]] [[As Low As is Reasonably Achievable]]
: [[AP]] [[]]
: [[AP]] [[]]
: [[ALARA]] [[Plan]]
: [[ALARA]] [[Plan]]
: [[AS]] [[]]
: [[ASME]] [[American Society of Mechanical Engineers]]
: [[ME]] [[American Society of Mechanical Engineers]]
: [[BACC]] [[Boric Acid Corrosion Control]]
: [[BA]] [[]]
: [[CC]] [[Boric Acid Corrosion Control]]
: [[BCO]] [[Basis for Continued Operations]]
: [[BCO]] [[Basis for Continued Operations]]
: [[BMI]] [[Bare Metal Inspection]]
: [[BMI]] [[Bare Metal Inspection]]
: [[BV]] [[]]
: [[BVPS]] [[Beaver Valley Power Station]]
PS  Beaver Valley Power Station
: [[CFR]] [[Code of Federal Regulations]]
CFR Code of Federal Regulations
: [[CR]] [[Condition Report(s)]]
CR Condition Report(s)
: [[DM]] [[Dissimilar Metal]]
DM Dissimilar Metal
: [[DPW]] [[Declared Pregnant Workers]]
DPW Declared Pregnant Workers
: [[EAL]] [[Emergency Action Level]]
: [[EAL]] [[Emergency Action Level]]
: [[ERF]] [[Emergency Response Facility]]
: [[ERF]] [[Emergency Response Facility]]
: [[FA]] [[Functionality Assessments]]
: [[FA]] [[Functionality Assessments]]
: [[FEN]] [[]]
: [[FENOC]] [[First Energy Nuclear Operating Company]]
: [[OC]] [[First Energy Nuclear Operating Company]]
: [[FOSAR]] [[Foreign Object Search and Retrieval]]
: [[FOS]] [[]]
: [[IOD]] [[Immediate Operability Determinations]]
AR Foreign Object Search and Retrieval
: [[IMC]] [[Inspection Manual Chapter]]
IOD Immediate Operability Determinations
: [[IP]] [[Inspection Procedure]]
IMC   Inspection Manual Chapter
IP Inspection Procedure
ISI  Inservice Inspection
ISI  Inservice Inspection
LCO  Limiting Conditions for Operations
LCO  Limiting Conditions for Operations
Attachment
Attachment
: [[LER]] [[Licensee Event Report]]
: [[LER]] [[Licensee Event Report]]
LHRA Locked High Radiation Area
: [[LHRA]] [[Locked High Radiation Area]]
MR Maintenance Rule
: [[MR]] [[Maintenance Rule]]
MRP Materials Reliability Program
: [[MRP]] [[Materials Reliability Program]]
MSP Maintenance Surveillance Package
: [[MSP]] [[Maintenance Surveillance Package]]
MT Magnetic Particle Testing
: [[MT]] [[Magnetic Particle Testing]]
NDE Non-Destructive Examination
: [[NDE]] [[Non-Destructive Examination]]
NRC Nuclear Regulatory Commission
: [[NRC]] [[Nuclear Regulatory Commission]]
: [[NRR]] [[Nuclear Reactor Regulation]]
: [[NRR]] [[Nuclear Reactor Regulation]]
: [[OD]] [[Operability Determinations]]
: [[OD]] [[Operability Determinations]]
OST Operations Surveillance Test
: [[OST]] [[Operations Surveillance Test]]
PI Performance Indicator
: [[PI]] [[Performance Indicator]]
PI&R Problem Identification and Resolution
: [[PI&R]] [[Problem Identification and Resolution]]
PMT   Post Maintenance Testing
: [[PMT]] [[Post Maintenance Testing]]
POD Prompt Operability Determinations
: [[POD]] [[Prompt Operability Determinations]]
PT Penetrant Testing
: [[PT]] [[Penetrant Testing]]
PWR Pressurized-Water Reactor
: [[PWR]] [[Pressurized-Water Reactor]]
RBC Reactor Building Containment
: [[RBC]] [[Reactor Building Containment]]
RCS Reactor Coolant System
: [[RCS]] [[Reactor Coolant System]]
RHR Residual Heat Removal
: [[RHR]] [[Residual Heat Removal]]
RSS Recirculation Spray System
: [[RSS]] [[Recirculation Spray System]]
: [[RWP]] [[Radiation Work Permit]]
: [[RWP]] [[Radiation Work Permit]]
: [[SAC]] [[Station]]
: [[SAC]] [[Station]]
ALARA Committee
: [[ALARA]] [[Committee]]
SSC Structures, Systems, and Components
: [[SSC]] [[Structures, Systems, and Components]]
SG Steam Generator
: [[SG]] [[Steam Generator]]
TS Technical Specification
: [[TS]] [[Technical Specification]]
: [[UE]] [[Unusual Event]]
: [[UE]] [[Unusual Event]]
: [[UFS]] [[]]
: [[UFSAR]] [[Updated Final Safety Analysis Report]]
AR Updated Final Safety Analysis Report
UT  Ultrasonic Testing
UT  Ultrasonic Testing
: [[VT]] [[Visual Testing]]
: [[VT]] [[Visual Testing]]
}}
}}

Revision as of 19:53, 25 August 2018

IR 05000334-09-003 & 05000412-09-003 on 04/01/09 - 06/30/09 for Beaver Valley
ML092160021
Person / Time
Site: Beaver Valley
Issue date: 08/04/2009
From: Bellamy R R
NRC/RGN-I/DRP/PB6
To: Sena P P
FirstEnergy Nuclear Operating Co
BELLAMY RR
References
IR-09-003
Download: ML092160021 (42)


Text

UNITED STATES NUCLEAR REGULATORY COMMISSION REGION I 475 ALLENDALE ROAD KING OF PRUSSIA, PA 19406-1415 August 4, 2009

Mr. Peter P. Sena, III Site Vice President FirstEnergy Nuclear Operating Company Beaver Valley Power Station P. O. Box 4, Route 168 Shippingport, PA 15077

SUBJECT: BEAVER VALLEY POWER STATION - NRC INTEGRATED INSPECTION REPORT 05000334/2009003 AND 05000412/2009003

Dear Mr. Sena:

On June 30, 2009, the United States Nuclear Regulatory Commission (NRC) completed an inspection at your Beaver Valley Power Station Units 1 and 2. The enclosed integrated inspection report documents the inspection results which were discussed on July 22, 2009, with members of your staff.

The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.

Based on the results of this inspection, this report documents one NRC-identified finding and one self-revealing finding, both of very low safety significance (Green). These findings were determined to involve violations of NRC requirements. Additionally, a licensee-identified violation which was determined to be of low safety significance is listed in this report. However, because of the very low safety significance and because the issues have been entered in the corrective action program, the NRC is treating the findings as non-cited violations (NCVs)

consistent with Section VI.A.1 of the NRC Enforcement Policy. If you contest any of the findings in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator Region I; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at Beaver Valley. In addition, if you disagree with the characterization of the cross-cutting aspect of any finding in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region 1 and the NRC Senior Resident Inspector at the Beaver Valley Power Station.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, and its enclosures, and your response (if any) will be available electronically for public ins pection in the P. Sena, III 2

NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Website at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

We appreciate your cooperation. Please contact me at 610-337-5200 if you have any questions regarding this letter.

Sincerely,/RA/

Ronald R. Bellamy, Ph.D., Chief Reactor Projects Branch 6 Division of Reactor Projects

Docket Nos.: 50-334, 50-412 License Nos: DPR-66, NPF-73

Enclosures:

Inspection Report 05000334/2009003; 05000412/2009003

w/Attachment:

Supplemental Information cc w/encl:

J. Hagan, President and Chief Nuclear Officer J. Lash, Senior Vice President of Operations and Chief Operating Officer D. Pace, Senior Vice President, Fleet Engineering

K. Fili, Vice President, Fleet Oversight P. Harden, Vice President, Nuclear Support G. Halnon, Director, Fleet Regulatory Affairs Manager, Fleet Licensing Company R. Lieb, Director, Site Operations D. Murray, Director, Maintenance M. Manoleras, Director, Engineering R. Brosi, Director, Site Performance Improvement C. Keller, Manager, Site Regulatory Compliance D. Jenkins, Attorney, FirstEnergy Corporation M. Clancy, Mayor, Shippingport, PA D. Allard, Director, PADEP C. O'Claire, State Liaison to the NRC, State of Ohio Z. Clayton, EPA-DERR, State of Ohio

Director, Utilities Department, Public Utilities Commission, State of Ohio D. Hill, Chief, Radiological Health Program, State of West Virginia J. Lewis, Commissioner, Division of Labor, State of West Virginia W. Hill, Beaver County Emergency Management Agency J. Johnsrud, National Energy Committee, Sierra Club P. Sena, III 3

NRC's document system (ADAMS). ADAMS is accessible from the NRC Website at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

We appreciate your cooperation. Please contact me at 610-337-5200 if you have any questions regarding this letter.

Sincerely,/RA/ Ronald R. Bellamy, Ph.D., Chief Reactor Projects Branch 6 Division of Reactor Projects

Distribution w/encl

S. Collins, RA M. Dapas, DRA D. Lew, DRP J. Clifford, DRP R. Bellamy, DRP G. Barber, DRP C. Newport, DRP J. Greives, DRP D. Werkheiser, DRP, SRI D. Spindler, DRP, RI P. Garrett, DRP, Resident OA L. Trocine, RI OEDO R. Nelson, NRR N. Morgan, PM, NRR R. Guzman, NRR S. West, DRS-RIII

C. Pederson, DRP-RIII ROPreportsResource@nrc.gov Region I Docket Room (with concurrences)

ML092160021 SUNSI Review Complete: RRB (Reviewer's Initials)

DOCUMENT NAME: G:\DRP\BRANCH6\+++BEAVER VALLEY\BV INSPECTION REPORTS & EXIT NOTES\ BV INSPECTION REPORTS 2009\BVREPORT-IR2009-003.DOC After declaring this document "An Official Agency Record" it will be released to the Public . To receive a copy of this document, indicate in the box:

" C" = Copy without attachment/enclosure " E" = Copy with attachment/enclosure " N" = No copy OFFICE RI/DRP RI/DRP NAME DWerkheiser/DW RBellamy/ RRB DATE 07/29/09 08/04/09 OFFICIAL RECORD COPY 1 Enclosure U. S. NUCLEAR REGULATORY COMMISSION REGION I

Docket Nos. 50-334, 50-412

License Nos. DPR-66, NPF-73

Report Nos. 05000334/2009003 and 05000412/2009003

Licensee: FirstEnergy Nuclear Operating Company (FENOC)

Facility: Beaver Valley Power Station, Units 1 and 2

Location: Post Office Box 4 Shippingport, PA 15077

Dates: April 1, 2009 through June 30, 2009

Inspectors: D. Werkheiser, Senior Resident Inspector D. Spindler, Resident Inspector J. Ayala, Resident Inspector P. Kaufman, Senior Reactor Inspector T. Moslak, Health Physicist O. Ayegbusi, Reactor Inspector

Approved by: R. Bellamy, Ph.D., Chief Reactor Projects Branch 6 Division of Reactor Projects

2 Enclosure TABLE of

SUMMARY OF FINDINGS

IR 05000334/2009003, IR 05000412/2009003; 04/01/2009 - 06/30/2009; Beaver Valley Power

Station, Units 1 & 2; Post-Maintenance Testing, Problem Identification and Resolution

The report covered a 3-month period of inspection by resident inspectors, regional reactor inspectors, and a regional health physics inspector. Two (GREEN) findings were identified. The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, ASignificance Determination Process

@ (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. Cross-cutting aspects associated with findings are determined using IMC 0305, "Operating Reactor Assessment Program," dated January 2009. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, AReactor Oversight Process,@ Revision 4, dated December 2006.

Cornerstone: Mitigating Systems

Green.

A non-cited violation (NCV) of 10CFR Part 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings" was identified for failure to specify and perform an adequate post-maintenance test (PMT) after replacing a safety-related river water check-valve. Specifically, the PMT under work order 200233562 was not adequate to verify the proper function of the valve 1RW-57 prior to its return to service. The PMT was subsequently performed successfully. This issue was entered into the licensee's corrective action program as condition report 09-59866.

The failure to specify and perform an adequate PMT after replacing a safety-related river water check-valve was a performance deficiency. The finding was more than minor in accordance with IMC 0612, Appendix B (Section 1-3), "Issue Screening," because the failure to specify and perform an adequate PMT is associated with the procedure quality performance attribute of the mitigating systems cornerstone and affects the associated cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences.

This finding has a cross-cutting aspect in the area of human performance associated with resources because the licensee did not have complete, accurate, and up-to-date maintenance work procedures [IMC 0305 Aspect:

H.2(c) (Section 1R19).

Green.

The inspectors identified a non-cited violation (NCV) of 10CFR Part 50, Appendix B, Crit erion III, "Design Control," in that FENOC failed to maintain safety-related cables in an environment for which they were designed. Since NRC Information Notice 2002-12 was issued, FENOC has had several opportunities to trend as-found data, implement effective maintenance programs, and identify and thoroughly evaluate long-term adverse conditions for underground safety-related cables exposed to continuous submerged environments. Cables affected include those for Unit 1 river water and Unit 2 service water. The issue was entered into the licensee's corrective action program (CR 09-60496) to initiate a review of the current manhole and cable monitoring programs, and to initiate long-term corrective actions.

Failure to maintain safety related cables in an environment for which they were designed is considered a performance deficiency. The finding was more than minor in accordance with IMC 0612, Appendix B (Section 1-3), "Issue Screening," because if left uncorrected, the performance deficiency has the potential to lead to a more significant safety concern.

Specifically, the deficiency did not result in the present loss of operability or functionality and did not represent a risk significant external event such as flooding. The issue was entered into the licensee's corrective action program (CR 09-60496) to initiate a review of the current manhole and cable monitoring programs, and to initiate long-term corrective actions.

The performance deficiency had a cross-cutting aspect in the area of Problem Identification and Resolution, Corrective Action Program, because the licensee did not thoroughly evaluate problems such as resolutions, address causes, and evaluate the effectiveness of corrective actions [IMC 0305 Aspect:

P.1 (c)] (Section 4OA2.3).

Other Findings

A violation of very low safety significance, which was identified by the licensee, has been reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensee's corrective action program. This violation and corrective actions are listed in Section 4OA7 of this report.

REPORT DETAILS

Summary of Plant Status

Unit 1 began the inspection period at 100 percent power. On April 1, the unit began a planned coastdown, on April 16 reduced power to 82 percent for planned condenser waterbox cleaning, and shut down on April 19 to commence a refueling outage (1R19).

On May 21, the unit was restarted and synchronized to the grid, achieving full power on May 24. The unit remained at 100 percent power for the remainder of the inspection period.

Unit 2 began the inspection period at 100 percent power. On April 18, the unit was down-powered to 97 percent for planned turbine valve testing and returned to full power later the same day. On May 30 through May 31 the unit was reduced to 96 percent to address first-point feedwater heater level control issues and returned to full power. The unit remained at 100 percent power for the remainder of the inspection period.

1.

REACTOR SAFETY

Cornerstone:

Initiating Events, Mitigating Systems, Barrier Integrity [R]

1R01 Adverse Weather Protection

.1 Seasonal Susceptibility

a. Inspection Scope

(2 samples - Hot Weather / Hurricane, Offsite and Alternate AC Power System Readiness)

The inspectors reviewed the Beaver Valley Power Station (BVPS) design features and FENOC's implementation of procedures to protect risk significant mitigating systems from adverse weather effects due to summer weather and hurricanes. The inspectors conducted interviews with various station personnel to gain insights into the station's hot weather and hurricane readiness and reviewed the status of various work orders categorized as warm weather preparation activities. The inspectors reviewed the corrective action program database, operating experience, and the Updated Final Safety Analysis Report (UFSAR), to determine the types of adverse weather conditions to which the site is susceptible, and to verify that the licensee was appropriately identifying and resolving weather-rela ted equipment problems.

The inspectors also reviewed BVPS design features and FENOC's implementation of procedures to handle issues that could impact offsite and alternating current (AC) power systems. The inspectors reviewed FENOC's procedures and programs which discussed

the operation and availability/reliability of offsite and alternate AC power sy stems during adverse weather. The inspectors verified that communication protocols between the transmission system operator and FENOC existed, and the appropriate information would be conveyed when potential grid stress and disturbances existed. The inspectors also verified that FENOC's procedures contained actions to monitor and maintain the availability/reliability of offsite and onsite power systems prior to and during adverse weather conditions.

b. Findings

No findings of significance were identified.

1R04 Equipment Alignment

.1 Partial System Walkdowns

a. Inspection Scope

(4 samples)

The inspectors performed four partial equipment alignment inspections during conditions of increased safety significance, including when redundant equipment was unavailable during maintenance or adverse conditions. The partial alignment inspections were also completed after equipment was recently returned to service after significant maintenance. The inspectors performed partial walkdowns of the following systems, including associated electrical distribution components and control room panels, to verify the equipment was aligned to perform its intended safety functions:

  • Unit 1, on April 16, train 'A' high head safety injection during the performance of 1OST-7.19D, "Safety Injection Relay Test (Slave Relay K610)-Train B;"
  • Unit 1, on April 21, train 'B' residual heat removal system while 'A' electrical train was cleared for maintenance; and
  • Unit 1, on April 29, containment penetrations during the core reload.

b. Findings

No findings of significance were identified.

.2 Complete System Walkdown

a. Inspection Scope

(2 samples)

The inspectors performed complete system walkdowns of the following systems to verify that the critical portions, such as valve positions, switches, and breakers, were correctly aligned in accordance with procedures, and to identify any discrepancies that may have had an effect on operability.

The inspectors also reviewed outstanding maintenance work orders to verify that the deficiencies did not significantly affect the system function. In addition, the inspectors discussed system health with the system engineer and reviewed the condition report database to verify that equipment alignment problems were being identified and appropriately resolved. Documents reviewed during the inspection are listed in the

.

  • On June 4, alignment and condition of the Unit 2 'C' service water pump and 'A' service water train while the 'D' main intake bay (affecting the 'A' service water pump) was out of service for planned cleaning; and
  • On June 6, alignment of 'A' and 'B' motor-driven auxiliary and dedicated feedwater pumps while the turbine-driven feedwater pump was out of service for planned maintenance.

b. Findings

No findings of significance were identified.

1R05 Fire Protection

.1 Quarterly Sample Review

a. Inspection Scope

(7 samples)

The inspectors reviewed the conditions of the fire areas listed below, to verify compliance with criteria delineated in Administrative Procedure 1/2-ADM-1900, "Fire Protection,"

Rev. 19. This review included FENOC's control of transient combustibles and ignition sources, material condition of fire protection equipment including fire detection systems, water-based fire suppression systems, gaseous fire suppression systems, manual firefighting equipment and capability, passive fire protection features, and the adequacy of compensatory measures for any fire protection impairments. Documents reviewed are listed in the Attachment:

  • Unit 2, TR-2C Unit Station Service Transformer (Fire Area TR-2);
  • Unit 2, TR-2D Unit Station Service Transformer (Fire Area TR-3);
  • Unit 1, AE Switchgear Room, Battery Rooms 1& 3 (Fire Area ES-1);
  • Unit 1, DF Switchgear Room, Battery Rooms 2& 4 (Fire Area ES-2);
  • Unit 1, Reactor Containment (Fire Area RC-1); and
  • Unit 1, Rod Control Motor Generator Room (Fire Area MG-1)

b. Findings

No findings of significance were identified.

.2 Annual Fire Drill Observation

a. Inspection Scope

(1 sample)

The inspectors observed personnel performance during response to an indicated fire in the Emergency Response Facility sub-stat ion (also see Section 40A3.1) by the fire brigade on June 18. The inspection evaluated the station's demonstration of readiness in fire fighting response. The inspectors observed the fire brigade members using protective clothing, turnout gear, and self-contained breathing apparatus and entering the fire area in a controlled manner. The inspectors also observed the fire fighting equipment brought to the fire scene to evaluate whether sufficient equipment was available to effectively control and extinguish the simulated fire. The inspectors evaluated whether the permanent plant fire hose lines were capable of reaching the fire area and whether hose usage was adequate. The inspectors observed the fire fighting directions and communications between fire brigade members. The inspectors verified that the pre-fire plan was used and observed the post-event critique to evaluate fact-finding, lessons-learned and whether any immediate deficiencies needed addressed.

b. Findings

No findings of significance were identified.

1R06 Flood Protection Measures

a. Inspection Scope

(1 sample - underground cables)

The inspectors reviewed a sample of internal flood protection measures regarding cables located in underground manholes. The inspectors selected a FENOC inspection of manholes 8A and 8B that contain Unit 1 and Unit 2 safety-related power and control cables near the main intake structure. These cable manholes are underground and also the focus of a focus problem identification and resolution review (see section 4OA2.3).

This review was conducted to evaluate FENOC's protection of the enclosed safety-related systems from internal flooding condition. The inspectors entered the confined area with FENOC personnel, inspected the manhole, and monitored licensee maintenance activities. The inspectors also reviewed the UFSAR, related internal flooding evaluations, and other related documents. The inspectors examined the as-found equipment and conditions to ensure that they remained consistent with those indicated in the design basis documentation, flooding mitigation documents, and risk analysis assumptions. Documents reviewed during the inspection are listed in the

.

b. Findings

One finding of significance was identified and documented in section 4OA2.3.

1R08 Unit 1 Inservice Inspection (IP 71111.08)

a. Inspection Scope

(1 sample)

The purpose of this inspection was to assess the effectiveness of the licensee's in-service inspection (ISI) program for monitoring degradation of the reactor coolant system boundary, risk significant piping system boundaries, and the containment boundary for Unit 1. The inspector assessed the inservice inspection activities using the criteria specified in the American Society of Mechanical Engineers (ASME) Boiler and Pressure Vessel Code,Section XI and applicable NRC Regulatory Requirements. The inspector selected a sample of nondestructive examination (NDE) activities from the Unit 1 in-service inspection plan for the 1R19 outage for observation, documentation and record review, and evaluation for compliance with the requirements of the BVPS Unit 1 Risk-Informed Inservice Inspection Program and ASME Section XI. A sample of activities associated with the repair/replacement of safety related pressure boundary components was also reviewed. The sample selection was based on the inspection procedure objectives, risk significance, availability, and specifically on components and systems where degradation would result in a significant challenge to the integrity of pressure boundary components. The inspector also conducted a review of TI 2515/172, Reactor Coolant System Dissimilar Metal Butt Welds for Beaver Valley Power Station Unit 1.

The inspector reviewed in-process NDE, examination data records, deficiency reports and interviewed NDE personnel to evaluate t he technician skills and performance, test equipment capabilities, and examination techniques and to verify that the activities, including calibration, set-up, examination techniques, data analysis, and that indications and defects were evaluated and dispositioned in accordance with ASME Boiler and Pressure Vessel Code, 2001 Edition to 2003 Addenda Section XI, relevant ASME Code Cases, selected relief requests, BVPS Unit 1 Risk-Informed Inservice Inspection Program, the Materials Reliability Program (MRP)recommendations, and compliance with 10CFR 50.55a.

The inspector also verified that observed indications and deficient conditions were being adequately entered and dispositioned in the BVPS corrective action program.

Non-Destructive Examination (NDE) and Welding Activities

The following dye penetrant testing (PT), ultrasonic testing (UT), magnetic particle testing (MT), and visual testing (VT) activities performed during 1R19 outage were reviewed by the inspector.

The inspector observed and reviewed a sample of NDE examinations and documentation records of manual UT examination of reactor coolant system (RCS) 'A' loop cold and hot leg nozzle-to-safe-end dissimilar metal (DM) welds RC-E-1A-N11 and RC-E-1A-N12 and RCS 'C' loop cold leg pipe girth weld DLW-LOOP3-7-S-02 performed as follow-up UT examination for a flaw indication initially identified in March 1996. The inspector reviewed visual bare metal inspections (BMI) records and photos of the Unit 1 reactor pressure vessel lower head penetration nozzles. The resident inspection staff directly observed VT boric acid walk-down inspections inside the Unit 1 containment.

The inspector also performed a document review of UT thickness examination data records of the Unit 1 containment liner, which was an examination in the area around a through-wall hole that was identified during 1R19 outage and magnetic particle and UT examinations of the liner replacement repairs, UT thickness examination data records of the Unit 1 containment liner area #3, and PT examination data record of residual heat removal (RHR) welded attachment RH-1-1-A-02.

Qualified FENOC inspectors visually examined the condition of accessible portions of the containment, including the inside surface of the containment liner for corrosion, mechanical damage and other degradation mechanisms during the 1R19 outage. As a result of an observed blister in the protective paint coating and protruding rust on the inside surface of the containment liner at the 738' elevation, a work order was written to clean the area to allow further evaluation. The cleaning activity uncovered a through-wall corrosion rectangular hole approximately 1" (horizontal) x 3/8" (vertical) in the containment liner which was documented in CR 09-57589 and 09-57762 and reported to the NRC per 10CFR50.72 on April 23, 2009. Manual UT thickness examinations of the containment liner of the affected area were taken as part of ASME Section XI, Subsection IWE to determine the extent of the liner corrosion. The inspectors observed various aspects of the containment liner NDE inspections, liner plate replacement, repair welding, and testing activities during the 1R19 outage. A more detailed inspection and assessment of the containment liner through-wall corrosion hole is documented in inspection report 05000334/2009006.

The inspector examined disposition for continued operation, without repair or rework, of non-conforming condition indications identified during 1R19 outage ISI activities. The inspector reviewed a liquid penetrant (PT) examination report PT-09-1003 and evaluation report EV-09-1002 of welded attachment RH-1-1-A-02, located on an RHR system elbow for spring can hanger SH-40, which identified a liner indication at the attachment/elbow interface area that wa s determined acceptable after light filling of the surface indication.

Repair/Replacement Consisting of Welding

Ultrasonic (UT) examinations performed on base material per the Materials Reliability Program (MRP) MRP-146 recommendations identified two circumferential indications approximately 3/8 inches in length in the stainless steel base material adjacent to a socket weld on the horizontal portion of BV-1RC-41, a 2-inch drain line connected to the "A" reactor coolant system (RCS) Hot Leg. The deficient condition was documented in CR 09-58004 and work order 200367565 was initiated to replace the affected piping segment of the 2-inch drain line. To verify suitability of materials, welding activities performed, applicable NDE performed, and ISI implementing procedures were in accordance with the ASME code requirements the inspector reviewed the work scope, activity sequence, weld filler metal selection, welding pr ocedure, non-destructive examination tests, acceptance criteria and post work testing.

Reactor Pressure Vessel Lower Head Penetration Nozzle Inspection

The inspector verified the inspection results of the visual BMI of the Unit 1 reactor pressure vessel lower head penetration nozzles that was conducted by VT-qualified FENOC personnel during 1R19 by reviewing visual inspection documentation record results and photos of the BMI inspection. No boric acid leakage was observed around the annulus area on the 43 penetrations inspected.

Pressurized Water Reactor Vessel Upper Head Penetration Inspection

No inspections were performed of the BVPS Unit 1 reactor vessel upper head during

1R19 outage because the Unit 1 reactor vessel head was replaced in 2006 during 1R17

outage. The inspector reviewed applicable NRC Regulatory Requirements and ASME Code,Section XI, to verify that no examinations were required of the Unit 1 reactor vessel upper head.

Boric Acid Corrosion Control (BACC) Inspection Activities

The inspector discussed the boric acid control program controlled by BVPS procedure NOP-ER-2001, Boric Acid Corrosion Control Program with the boric acid corrosion control program owner and sampled photographic inspections of boric acid found on safety significant piping and components inside Unit 1containment during Mode 3 walk downs conducted by FENOC personnel in April 2009. The walk down was directly observed by the resident inspection staff, to verify that the visual inspections were performed in accordance with the procedure and checklists which emphasized the areas and locations where boric acid leaks could cause degradation of safety significant components and that deficient conditions were identified and documented.

Approximately 138 locations were identified with boric acid during 1R19 walk down inspections.

A sample of engineering evaluations/corrective actions associated with these boric acid deficiencies and a sample of these items on the Unit 1 mode hold list were reviewed by the inspector. The inspector confirmed that condition reports were assigned corrective actions consistent with the requirements of the ASME Code and 10 CFR 50, Appendix B, Criterion XVI. The inspector reviewed various condition reports and work orders to resolve the identified deficient boric acid conditions.

Steam Generator (SG) Tube Inspections The inspectors reviewed the BVPS Unit 1 1R18 steam generator degradation assessment SG-CDME-07-24. No inspections were performed of the BVPS Unit 1 steam generator tubes during 1R19 outage because the Unit 1 steam generators were replaced in 2006 during 1R17 outage. The inspector reviewed applicable NRC Regulatory Requirements and the ASME Code Section XI to verify that no examinations were required during 1R19.

Problem Identification and Resolution The inspector reviewed a sample of condition reports related to ISI, MRP-139, and MRP-146 program activities to assess FENOC's effectiveness in problem identification and resolution and determined that deficiencies are being appropriately identified, and entered into and resolved by the corrective action program.

1R11 Licensed Operator Requalification Program

a. Inspection Scope

(1 sample)

The inspectors observed Unit 2 licensed operator simulator training on June 23. The inspectors evaluated licensed operator performance regarding command and control, implementation of normal, annunciator response, abnormal, and emergency operating procedures, communications, technical specification review and compliance, and emergency plan implementation. The inspectors evaluated the licensee staff training personnel to verify that deficiencies in operator performance were identified, and that conditions adverse to quality were entered into the licensee's corrective action program for resolution. The inspectors reviewed simulator physical fidelity to assure the simulator appropriately modeled the plant control room. The inspectors verified that the training evaluators adequately addressed that the applicable training objectives had been achieved.

b. Findings

No findings of significance were identified.

1R12 Maintenance Rule Implementation

a. Inspection Scope

(2 samples)

The inspectors evaluated Maintenance Rule (MR) implementation for the issues listed below. The inspectors evaluated specific attributes, such as MR scoping, characterization of failed structures, systems, and components (SSCs), MR risk characterization of SSCs, SSC performance criteria and goals, and appropriateness of corrective actions. The inspectors verified that the issues were addressed as required by 10 CFR 50.65 and the licensee's program for MR implementation. For the selected SSCs, the inspectors evaluated whether performance was properly dispositioned for MR category (a)(1) and (a)(2) performance monitoring. MR System Basis Documents were also reviewed, as appropriate.

  • Unit 1, Solid State Protection System does not achieve MR a(1) goals, as documented in CR 09-59359; and
  • Unit 1, 1CCP-P-1A, head ratio greater than acceptance criteria as documented in CR 09-60127.

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessment and Emergent Work Control

a. Inspection Scope

(5 samples)

The inspectors reviewed the scheduling and control of five activities, and evaluated their effect on overall plant risk. This review was conducted to ensure compliance with applicable criteria contained in 10 CFR 50.65(a)(4). Documents reviewed during the inspection are listed in the Attachment.

  • On April 20, Unit 1 refueling outage defense-in-depth report re-assessment for changes in calculated time-to-boil values, as document in CR 09-57463;
  • On April 21, Unit 1 yellow shutdown risk during EDG 1-1 autoload test;
  • Week of June 1, Unit 1 and Unit 2, review of station risk during planned 'D' main intake bay cleaning; and
  • During June 15-21, Unit 1 and Unit 2, review of changed and emergent work coordination for that planned week's activities, including a review of station processes and procedures for risk determination.

b. Findings

No findings of significance were identified.

1R15 Operability Evaluations

a. Inspection Scope

(6 samples)

The inspectors evaluated the technical adequacy of se lected immediate operability determinations (I OD), prompt operability determinations (POD), or functionality assessments (FA), to verify that determinations of Technical Specifications (TS)operability were justified, as appropriate. In additi on, the inspectors verified that TS limiting conditions for operation (LCO) requirements and UFSAR design basis requirements were properly addressed. In addition, the inspectors reviewed compensatory measures implemented to ensure the measures worked and were adequately controlled. Documents reviewed are listed in the Attachment.

  • April 12 -14, Unit 1 turbine-driven auxiliary feedwater pump (FW-P-2) steam isolation valve (MOV-1MS-105) failed to open electrically as documented in CR 09-57106;
  • On April 21, Unit 1 primary component cooler inlet temperature indicator failure to containment penetration cooling coils documented in CR 09-57667;
  • On April 23, Unit 1 containment liner plate degradation documented in CRs 09-57589, 09-57762;
  • On June 16, Unit 2 licensee's functional assessment regarding fire protection safe shutdown report analysis of station air documented in CRs 09-60058, 09-60162, 06-6932.

b. Findings

No findings of significance were identified.

1R18 Plant Modifications

.1 Temporary Plant Modifications

a. Inspection Scope

(2 samples)

The inspectors reviewed the following temporary modifications (TMOD) based on risk significance. The TMOD and associated 10 CFR 50.59 screening were reviewed against the system design basis documentation, including the UFSAR and the TS. The inspectors verified the TMODs were implemented in accordance with Administrative (ADM) Procedure, 1/2-ADM-2028, "Temporary Modifications," Rev. 9. Documents reviewed are listed in the Attachment.

  • TMOD ECP 09-01453 to provide additional mitigating configuration and control of plant operations during solid plant operation while shutdown.

b. Findings

No findings of significance were identified.

.2 Permanent Plant Modifications

a. Inspection Scope

(1 sample)

The inspectors evaluated the design basis impact of the modification to the Unit 1 reactor trip breaker circuit under ECP 08-0134-002. The inspectors reviewed the adequacy of the associated 10 CFR 50.59 screening, verified that attributes and parameters within the design documentation were consistent with required licensing and design bases, as well as credited codes and standards, and observed portions of the modification to verify that changes described in the package were appropriately implemented. The inspectors also verified the post-modification testing was satisfactorily accomplished to ensure the system and components operated consistent with their intended safety function.

Documents reviewed are listed in the Attachment.

b. Findings

No findings of significance were identified.

1R19 Post-Maintenance Testing

a. Inspection Scope

(7 samples)

The inspectors reviewed the following activities to determine whether the post-maintenance tests (PMT) adequately demonstrated that the safety-related function of the equipment was satisfied given the scope of the work, and that operability of the system was restored. In addition, the inspectors evaluated the applicable acceptance criteria to verify consistency with the design and licensing bases, as well as TS requirements. The inspectors witnessed the test or reviewed test data to verify results adequately demonstrated restoration of affected safety functions. The inspectors also verified that conditions adverse to quality were entered into the corrective action program for resolution. Documents reviewed during the inspection are listed in the Attachment.

  • On April 3, 1OST-30.3, after planned maintenance on Unit 1 'B' train river water;
  • On April 14, Unit 1, new-fuel frame hoist motor (1FN-W-1-MOTOR) cable replacement;
  • On April 21, Unit 1, replacement and retest of VSR2 in No.1-1 emergency diesel output breaker (4KVS-1AE-1E9) control circuit;
  • On May 8, Unit 1, final painting and baseline volumetric scan after containment plate liner repair;
  • On May 19, Unit 1, replacement of number 2 seal on 'A' reactor coolant pump; and

b. Findings

Introduction:

A self-revealing Green NCV of 10CFR Part 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings" was identified for failure to specify and perform an adequate PMT after replacing a safety-related river water check-valve. Specifically, train 'A' river water was declared operable after replacement of check valve 1RW-57 per work order 200233562 without an adequate PMT.

Description:

On May 25, 2009, the 'A' main intake bay was removed from service for planned bay cleaning. This rendered the 'A' safety-related river water pump (1WR-P-1A)inoperable. The spare 'C' river water pump (1WR-P-1C) was aligned to service the 'A' river train. During the bay cleaning, the 'A' river water pump discharge check valve (1RW-57) was replaced on May 28 by mechanical maintenance per work order 200233562. This work order did not specify PMT requirements. The work order was signed complete and the 'A' intake bay was returned to service on May 28. On May 29 the 'A' river water train was re-aligned, placing the 1WR-P-1A pump in service and operable at 12:25 p.m. At 2:40 p.m., it was identified that PMT was not performed for replacement of 1RW-57. The shift manager immediately declared 'A' train river water inoperable and aligned the WR-P-1C to serve the 'A' river water train.

The inservice testing coordinator was contacted to identify post-maintenance testing requirements. ASME OM Code, Section ISTC-5221 requires a forward flow and reverse-closure verification for post-maintenance testing following a check valve replacement.

The PMT was accomplished satisfactorily on June 1.

The licensee's post-maintenance process failed to specify an adequate PMT for the check valve replacement. The work order lacked any operational PMT and was the apparent cause of the performance deficiency. The licensee documented this issue in CR 09-59866.

Analysis:

The failure to specify and perform a PMT after replacing a safety-related river water check-valve was a performance deficiency. The inspectors determined that the performance deficiency was not similar to the examples for minor deficiencies contained in IMC 0612, Appendix E, "Examples of Minor Issues". The finding was more than minor in accordance with IMC 0612, Appendix B (Section 1-3), "Issue Screening," because the failure to specify and perform a PMT is associated with the procedure quality performance attribute of the mitigating systems cornerstone and affects the associated

cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences.

In accordance with IMC 0609.04 (Table 4a), "Phase 1 - Initial Screening and Characterization of Findings," the finding was determined to be of very low safety significance (Green) because the finding was not a design or qualification deficiency which resulted in a loss of function.

This finding has a crosscutting aspect in the area of human performance associated with resources because the licensee did not have complete, accurate, and up-to-date maintenance work procedures H.2(c).

Enforcement:

10 CFR 50, Appendix B, Criterion V, requires, in part, that procedures for performing maintenance that can affect the performance of safety-related equipment should be properly preplanned and performed in accordance with written procedures, documented instructions, or drawings appropriate to the circumstances. Contrary to this requirement, in May 2009, FENOC failed to specify and perform PMT after replacement of check value 1RW-57 prior to returning the system to operable status. Because this deficiency is considered to be of very low safety significance (Green), and was entered into the corrective action program (CR 09-59866), this violation is being treated as an NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy. (NCV 5000334/2009003-01, Inadequate Post-Maintenance Testing Specified for Safety-Related River Water Check Valve)

1R20 Refueling and Outage Activities

.2 Unit 1 Refueling Outage (1R19)

a. Inspection Scope

(1 sample)

The inspectors observed selected Unit 1 outage activities to determine whether shutdown safety functions (e.g. reactor decay heat removal, spent fool pool cooling, and containment integrity) were properly maintained as required by TS and plant procedures. The inspectors evaluated specific performance attributes including operator performance, communications, and instrumentation accuracy. The inspectors reviewed procedures and/or observed selected activities associated with the refueling outage. The inspectors verified activities were performed in accordance with procedures and verified required acceptance criteria were met. The inspectors also verified that conditions adverse to quality identified during performance of selected outage activities were identified by the licensee's corrective action program. Documents reviewed are listed in the Attachment. The inspectors also evaluated the following activities:

  • Pre-outage shutdown safety review / defense-in-depth reports;
  • Pre-outage temperature and power coastdown;
  • Reactor plant shutdown and cooldown, including evaluation of cooldown rates;
  • Solid plant operations;
  • Configuration management, compliance with TS when taking equipment out of service;
  • Implementation of clearance activities and confirmation that tags were hung properly;
  • Status and configuration of electrical systems and switchyard activities;
  • Fuel handling and activities that could affect reactivity;
  • Final containment walkdown and closeout inspection;
  • The digital video documenting the core reload and verification that fuel assembly placement was consistent with the reload map;
  • Subsequent shutdown and cooldown to replace 'A' reactor coolant pump seals after initial startup for physics testing; and
  • Final startup and power ascension to full power.

During the refueling outage FENOC identified a degradation of the containment liner during planned containment inspections. The review of this issue is documented in a separate report 05000334 / 2009006 (ADAMS ML091870328, on July 6, 2009). The inspectors also verified that refueling outage activities were in compliance with TS during

the containment liner repair and retest. This issue was also reviewed for operability (section 1R15, 1R19) and event follow-up (section 4OA3.1)

The inspectors also observed selected management review activities associated with restart readiness of Unit 1, following completion of the 1R19 refueling activities. The restart readiness review meeting was accomplished as required by NOBP-OM-4010, "Restart Readiness for Plant Outages" Rev. 4, during the week of May 11. The purpose of the review, in part, was to assure that the plant's material condition, programs/processes, and personnel were ready for startup and safe, reliable operation after completion of outage activities.

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing

a. Inspection Scope

(8 samples: 1 isolation valve, 1 leak rate, 1 in-service testing and 5 routine.)

The inspectors witnessed the performance of or reviewed test data for the eight following Operation Surveillance Test (OST) and Maintenance Surveillance (MSP) packages. The reviews verified that the equipment or systems were being tested as required by TS, the UFSAR, and procedural requirements. The inspectors also verified that the licensee established proper test conditions, that no equipment pre-conditioning activities occurred, and that acceptance criteria were met.

  • On March 26, 1OST-13.7B, Rev. 4, "Containment Depressurization System Operating Surveillance Test" [in-service testing];
  • On April 14, 1OST-1.04A, Rev. 0, "Train B, CIA On-line Valve Relay Test" [isolation valve];
  • On April 15, 1OST-36.2, Rev. 51, "Diesel Generator No. 2 Monthly Test";
  • On April 20, 1OST-36.04, Rev. 25, "Diesel Generator No. 2 Automatic Test";
  • On June 6, 1OST-15.1, Rev. 22, "[1CC-P-1A] Quarterly Test";
  • On May 10, 1OST-47.2B, Rev. 8, "Containment Closeout Inspection"; and

b. Findings

No findings of significance were identified. 2.

RADIATION SAFETY

Cornerstone:

Occupational Radiation Safety [OS]

2OS1 Access Control to Radiologically Significant Areas (71121.01)

a. Inspection Scope

(10 samples)

During the period April 27 - 30, the inspector conducted the following activities to verify that the licensee was properly implementing physical, administrative, and engineering controls for access to locked high radiation areas, and other radiologically controlled areas during the Unit 1 refueling outage. Implementation of these controls was reviewed against the criteria contained in 10 CFR 20, relevant TS, and the licensee's procedures.

This inspection activity represents the completion of ten (10) samples relative to this inspection area.

Plant Walkdown and Radiation Work Permits (RWP) Reviews

  • The inspector toured accessible radiologically controlled areas in the Unit 1 reactor building containment (RBC), primary auxiliary building, and radwaste building and with the assistance of a radiation protection technician, performed independent radiation surveys of selected areas to confirm the accuracy of survey data, and the adequacy of postings. Radiation protection technicians were questioned regarding their knowledge of plant radiological conditions for selected jobs, and the associated controls.
  • The inspector identified radiologically significant jobs being performed in the Unit 1 RBC. The inspector reviewed the applicable RWPs, ALARA Plans (AP), and the electronic dosimeter dose/dose rate set points, for the associated tasks, to determine if the radiological controls were acceptable and if the set points were consistent with plant policy. Jobs reviewed included steam generator sludge lancing (RWP 109-4015, AP 09-1-24), insulation removal/replacement (RWP 109-4032, AP 09-1-29),

remove/replace core exit thermocouples (RWP 109-4019, 09-1-26), and in-service inspections (RWP 109-4023, AP 09-1-29).

  • For the jobs reviewed, the inspector determined that there were no significant dose gradients requiring relocation of dosimetry. The inspector determined that tele-dosimetry was extensively used to monitor and control worker exposure for dose intensive jobs.
  • There were no current radiation work permits for airborne radioactivity areas with the potential for individual worker internal exposures to exceed 50 mrem during the 1R19 outage. The inspector reviewed air sampling records for ongoing jobs to confirm that airborne contamination was insignificant.
  • The inspector evaluated the effectiveness of contamination controls by reviewing personnel contamination event reports (and related condition reports), and observing practices at various work locations in the RBC and at the step off pad.

High Radiation Area and Very High Radiation Area Controls

  • The inspector reviewed procedures related to the control of high dose rate, high radiation area and very high radiation areas. The inspector discussed these procedures with Radiation Protection Supervision to determine that any changes made to these procedures did not reduce safety measures.
  • The inspector reviewed the preparations made for various potentially high dose rate jobs including removal of core exit thermocouples, and insulation modifications made to various systems in the RBC. Included in this review were evaluating the effectiveness of contamination control measures, source term controls, and use of temporary shielding.

Radiation Worker and Radiation Protection Technician Performance

  • During tours of radiologically controlled areas in the Unit 1 RBC, the inspector questioned radiation workers and radiation protection technicians regarding the radiological conditions at the work site and the radiological controls that applied to their task. Additionally, radiologically-related condition reports, including dose/dose rate alarm reports, were reviewed to evaluate if the incidents were caused by repetitive radiation worker or technician errors and to determine if an observable pattern traceable to a similar cause was evident.
  • The inspector attended the pre-job RWP briefings for a spent resin transfer, and for steam generator foreign object search and retrieval (FOSAR) to determine if workers were properly informed, including discussions of past operating experiences, identification of the radiological conditions associated with their tasks, electronic dosimetry dose/dose rate set points, and dose mitigation measures.

Problem Identification and Resolution

  • The inspectors evaluated the licensee's program for assuring that access controls to radiologically significant areas were effective and properly implemented by reviewing various Nuclear Oversight Field Observation Reports, radiation protection supervisory daily logs, and relevant condition reports. The inspector determined if problems were identified in a timely manner, that an extent of condition and cause evaluation were performed when appropriate, previous radiation surveys remained valid, and corrective actions were appropriate to preclude repetitive problems.

b. Findings

No findings of significance were identified.

2OS2 ALARA Planning and Controls (71121.02)

a. Inspection Scope

(9 samples)

During the period April 27 - 30, the inspector conducted the following activities to verify that the licensee was properly implementing operational, engineering, and administrative controls to maintain personnel exposure as low as is reasonably achievable (ALARA) for activities performed in the 1R19 refueling outage. Implementation of these controls was reviewed against the criteria contained in 10 CFR 20, and the licensee's procedures.

This inspection activity represents the completion of nine (9) samples relative to this inspection area.

Radiological Work Planning

  • The inspector reviewed pertinent information regarding site cumulative exposure history, current exposure trends, and the ongoing exposure challenges for the Unit 1 outage. The inspector reviewed the 1R19 Outage ALARA Plan.
  • The inspector reviewed the exposure status for tasks performed during the Unit 1 outage and compared actual exposure with forecasted estimates contained in various project ALARA Plans (AP). The inspector reviewed the Work-In-Progress ALARA reviews for those jobs whose actual dose approached 75% of the forecasted estimate. Outage jobs reviewed included scaffolding installation (AP 09-1-35),

insulation modifications (AP 09-01-33), reactor disassembly/reassembly (AP 09-1-25), routine valve work (AP 09-1-41), and replacing incore detectors (AP 09-1-19).

  • The inspector evaluated the departmental interfaces between radiation protection, operations, maintenance crafts, and engineering to identify missing ALARA program elements and interface problems. The evaluation was accomplished by interviewing site staff, reviewing outage Work-in-Progress reviews, attending a Station ALARA Committee (SAC) meeting, and reviewing SAC meeting minutes. The SAC meeting addressed planning for cutting/replacing a reactor coolant drain line (RC-41), and revising the exposure estimate for insulation modifications.

Verification of Dose Estimates

  • The inspector reviewed the assumptions and basis for the 1R19 outage ALARA plan. The inspector also reviewed the revisions made to various outage project dose estimates due to emergent work; e.g., insulation modifications (RWP 109-4048),

authorized by the Station ALARA Committee.

  • The inspector reviewed the licensee's procedures associated with monitoring and re-evaluating dose estimates when the forecasted cumulative exposure for tasks was approached and the implementation of these procedures during the outage. The inspector reviewed the exposures for the ten (10) workers who received the highest doses to confirm that no individual exceeded any regulatory limit.

Job Site Inspections

  • The inspector reviewed the ALARA controls specified for transferring resin from CH-I-1A to a disposal container (RWP 109-0507,AP 09-1-58, procedure 1/2 -HPP-3.03.007), and attended the pre-job ALARA briefing. The inspector also reviewed the controls used for manually transferring a spent filter (CH-FL-2) to a storage drum (RWP 109-1020, AP 09-1-11, procedure 1/2 OM-18.4A.E), the trouble shooting plan for removing the filter when it became disengaged from the transfer grapple, and the post-job debrief.
  • During tours of the RBC, the inspector observed workers performing steam generator sludge lancing/FOSAR (RWP 109-4015), eddy current testing on the recirculation spray heat exchanger (RWP 109-4043), valve repairs, and de-mobilization activities. Workers were questioned regarding their knowledge of job site radiological conditions and ALARA measures applied to their tasks.

Source Term Reduction and Control

  • The inspector reviewed the status and historical trends for the Unit 1 source term. Through review of survey maps and interviews with the Senior Nuclear Specialist-ALARA, the inspector evaluated recent source term measurements and control strategies. Specific strategies being employed included use of macro-porous clean up resin, zinc addition, increased filtration flow, enhanced chemistry controls, system flushes, and temporary shielding.

Declared Pregnant Workers

  • The inspector reviewed the procedural controls for managing declared pregnant workers (DPW) and determined that no DPW was employed during the Unit 1 outage. Problem Identification and Resolution
  • The inspector reviewed elements of the licensee's corrective action program related to implementing the ALARA program to determine if problems were being entered into the program for timely resolution. Condition reports related to programmatic dose challenges, personnel contaminations, and the effectiveness in predicting and controlling worker exposure were reviewed.

b. Findings

No findings of significance were identified.

OTHER ACTIVITIES

[OA]

4OA1 Performance Indicator Verification

a. Inspection Scope

(6 samples total)

The inspectors sampled licensee submittals for Performance Indicators (PI) listed below for both Unit 1 and Unit 2 to verify accuracy of the data recorded from April 2007 through June 2009. The inspectors reviewed Licensee Event Reports, condition reports, portions of various plant operating logs and reports, and PI data developed from monthly

operating reports. Methods for compiling and reporting the PIs were discussed with cognizant engineering and licensing personnel. To verify the accuracy of the PI data reported during this period, PI definitions and guidance contained in Nuclear Energy Institute (NEI) 99-02, "Regulatory Assessment Indicator Guideline," Revision 5, were used for each data element.

Cornerstone:

Mitigating Systems (2 samples)

  • Unit 1 and 2 Safety System Functional Failure [MS05]

Cornerstone:

Barrier Integrity (4 samples)

b. Findings

No findings of significance were identified.

4OA2 Problem Identification and Resolution (71152 - 2 samples total)

.1 Daily Review of Problem Identification and Resolution

a. Inspection Scope

As required by Inspection Procedure 71152, "Identification and Resolution of Problems,"

and in order to help identify repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed a daily screening of items entered into FENOC's corrective action program. This review was accomplished by reviewing summary lists of each CR, attending screening meetings, and accessing FENOC's computerized CR database.

b. Findings

No findings of significance were identified.

.2 Annual Sample: Review of Final Cause and Corrective Actions of Inadvertent Unlatch of a Control Rod Drive Shaft during Refueling 2R13

a. Inspection Scope

(1 sample)

The inspectors selected CR 08-39693 as a problem identification and resolution (PI&R)sample for a detailed follow-up review. CR 08-39693 documented on May 2, 2008, an inadvertent unlatching of a control rod drive shaft during its transfer from its storage location to its core location by vendor personnel after planned split pin replacements.

The tool used in the drive shaft installation was specific to the split pin replacement project. Review of the initial event is documented in report 05000412 / 2008003.

The inspectors reviewed the vendor apparent cause and assessed FENOC's cause analysis, extent of condition, operability determination, and prioritization and timeliness of corrective actions to prevent recurrence. Documents reviewed for this inspection are located in the Attachment.

b. Findings and Observations

No findings of significance were identified.

The inspectors determined that FENOC properly evaluated the degraded condition and implemented appropriate immediate and long term corrective actions. The CR was complete and included cause evaluations by FENOC and the vendor. No human performance deficiencies were noted. It was determined that the handing tool is not fail-safe and can unlatch if the drive shaft weight is relieved by interference with a guide card. The licensee discontinued use of the vendor's special tool during the issue and has revised applicable procedures to prevent future use.

.3 Annual Sample: Review of Submerged Safety Related Cables

a. Inspection Scope

(1 sample)

The inspectors selected CR 08-42380 as a PI&R sample for a detailed follow-up review. CR 08-42380 documented the identification of safety related cables found submerged in water on June 25, 2008 for an indefinite period of time. The issue was identified during routine manhole inspections. The inspectors assessed FENOC's problem identification threshold, operability determination, extent of condition review, and the prioritization and timeliness of corrective actions to determine whether FENOC was appropriately identifying, characterizing, and correcting problems associated with these issues and whether the planned or completed corrective actions were appropriate to prevent recurrence. Additionally, the inspectors observed manhole and cable inspections on June 9-10, 2009 and interviewed engineering personnel. The inspectors reviewed the specification, testing and long term moisture resistance qualification report for the subject cables. Specific documents reviewed are listed in the attachment to this report.

b. Findings and Observations

Introduction:

The inspectors identified a non-cited violation (NCV) of 10CFR Part 50, Appendix B, Criter ion III, "Design Control," in that FENOC did not maintain safety related cables in an environment for which they were designed. The licensee failed to demonstrate that the cables are qualified for continuous submerged conditions, and that they will remain operabl e, although t he cables are presently operable.

Description:

Safety related and non-safety related power and control cables may be submerged in water on a continuous basis. The affected cables included cables from the Unit 1 River Water and Unit 2 Service Water from the Main Intake Structure carrying power to the Class 1E load through electrical manholes 1EMH-8A and 1EMH-8B.

A review of the licensing basis and licensee documentation reveals the cables are selected and purchased for dry, wet, and immersed in water conditions. The inspectors determined, after discussions with additional NRC specialists, that this does not include continuous submerged conditions. The inspectors reviewed the specifications used to purchase these cables and noted that the subject cables are not designed for continuous submergance.

The environmental conditions in the manholes can be dry, wet, and immersed in water.

A review of the licensee's underground cable duct drawings showed that the manholes are constructed below grade and expected to accumulate water. However, the cables can become continuously submerged in water if the accumulation is not managed or manhole degraded conditions not effectively corrected. Presently, the licensee relies on cable penetration seal integrity and manual dewatering of the manholes annually (for 1EMH-8A and 8B only) or biennially to manage water accumulation. The most recent inspection (June 9, 2009) of manholes identified approximately 2 feet of water in 1EMH-8A and 11 feet of water in 1EMH-8B; conditions of apparent continuous submergence for manhole 1EMH-8B cables. The licensee failed to ensure that the cables were maintained in a design condition for the anticipated environmental conditions by not thoroughly evaluating the effect of continuous cable submergence apparent in CRs 09-60591; 08-43594; 08-42380; 06-6305; 06-04144; 04-03545; 02-02348 and evaluating the effectiveness of prior corrective actions.

The licensee had previously doc umented an engineering evaluation of cable suitability to submerged conditions (CR 02-02348, March 21, 2002) to address NRC Information Notice 2002-12, Submerged Safety-Related Electrical Cables. The licensee concluded that based on cable construction, qualification testing performed, and operational performance, the cables in manholes 1EMH-8A and 8B were acceptable. This evaluation had also been the basis for subsequent evaluations for as-found manhole conditions. Corrective actions were taken to annually inspect and dewater the manholes and address as-found degraded conditions, however the licensee has not adequately addressed the apparent continuous submergence of safety related cables in the subject manholes.

The licensee has pumped down water from the manholes to minimize water, and

inspected the cables, seals, and tray supports. An immediate operability assessment was also performed for as found conditions and CRs written (09-60316; 09-60445; 09-60591). The inspectors questioned the licensee on the need to re-evaluate the frequency of manhole inspections, based on as-found conditions.

A review of the licensee's response to NRC Generic Letter 2007-01, "Inaccessible or Underground Power Cable Failures that Disable Accident Mitigation Systems or Cause Plant Transients," did not identify any past cable failures at Beaver Valley.

Analysis:

Failure to maintain safety related cables in an environment for which they were designed is considered a performance deficiency. The inspectors determined that the performance deficiency was not similar to the examples for minor deficiencies contained in IMC 0612, Appendix E, "Examples of Minor Issues". The finding was more than minor in accordance with IMC 0612, Appendix B (Section 1-3), "Issue Screening," because if left uncorrected, the performance deficiency has the potential to lead to a more significant safety concern. Traditional enforcement does not apply since there were no actual safety consequences or potential for impacting the NRC's regulatory function, and the finding did not have willful aspects.

In accordance with IMC 0609.04 (Table 4a), "Phase 1 - Initial Screening and Characterization of Findings," the finding was determined to be of very low safety significance (Green) because the finding was not a design or qualification deficiency which resulted in a loss of operability or functionality, did not represent a loss of system safety function, did not represent an actual loss of safety function of a single train for greater than its technical specification allowed outage time, did not represent an actual loss of safety function of one or more non-technical specification trains of equipment designated as risk-significant for greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />, and was not potentially risk significant due to a seismic, flooding or severe weather initiating event.

The performance deficiency had a cross-cutting aspect in the area of Problem Identification and Resolution, Corrective Action Program, because the licensee did not thoroughly evaluate problems such as the resolutions, address causes, and evaluate the effectiveness of corrective actions [P.1 (c)].

Enforcement:

Title 10 CFR Part 50, Appendix B, Crit erion III, "Des ign Control," requires, in part, that measures shall be established to ensure that applicable regulatory requirements and the design basis are correctly translated into specifications, drawings, procedures, and instructions. Contrary to the above, FENOC did not maintain safety related cables in an environment for which they were designed. The issue was entered into the licensee's corrective action program (CR 09-60496) to initiate a review of the current manhole and cable monitoring programs, and to initiate long-term corrective actions. Because this finding was of very low safety significance, and it was entered into the licensee's corrective action program, this violation is being treated as an NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy. (NCV 05000334, 412/2009003-02, Continuously Submerged Cables Design Deficiency)

4OA3 Followup of Events and Notices of Enforcement Discretion (71153 - 7 samples total)

.1 Plant Event Review

a. Inspection Scope

(6 samples)

For the plant events below, the inspectors reviewed and/or observed plant parameters, reviewed personnel performance, and evaluated performance of mitigating systems.

The inspectors communicated the plant events to regional personnel and compared the event details with criteria contained in IMC 0309, "Reactive Inspection Decision Basis for Reactors," for consideration of additional reactive inspection activities. The inspectors reviewed FENOC's follow-up actions related to the events to assure that appropriate corrective actions were implemented commensurate with their safety significance.

Documents reviewed during the inspection are listed in the Attachment.

  • Unit 1: On April 20, 2009, main feedwater isolation (P14 actuation on high 'B' steam generator water level) during plant shutdown for refueling outage 1R19.

The high steam generator water level was caused by a failed main feedwater bypass regulating valve (1FW-489) controller, causing it to inadvertently fully open. Operators responded appropriately and mitigating systems performed as designed. The licensee documented this issue in CR 09-57474. This issue was also reviewed under NRC OpESS FY2009-02, "Negative Trend and Recurring Events Involving Feedwater Systems;"

  • Unit 1: On April 20, 2009, invalid actuation of the steam-driven auxiliary feedwater pump (FW-P-2) during plant shutdown for refueling outage 1R19. An apparent failed solid state protection relay caused one of two steam admission valves (TV-1MS-105B) to open, causing the pump to inject. The auxiliary feedwater flow control system responded appropriately to mitigate the effect on plant cooldown.

The licensee documented this issue in CR 09-57499. This issue was also reviewed under NRC OpESS FY2009-02, "Negative Trend and Recurring Events Involving Feedwater Systems;"

  • Unit 1: On April 23, 2009, identification of a degraded containment liner plate during a planned visual inspection in refueling outage 1R19. The degradation was repaired and declared operable on May 7, 2009. The licensee documented this issue in CRs 09-57589 and 09-57762. Also see section 1R08, "Inservice Inspection." This issue is documented in NRC Inspection Report 05000334/2009006 (ADAMS ML091870328, on July 6, 2009);
  • Unit 1: On April 26, 2009, identification of two circumferential ultrasonic examination indications on base material of a 2 inch reactor coolant loop drain line (BV-1RC-41) on the 'A' loop hot leg. The drain line material was replaced and returned to service. Also see section 1R08, "Inservice Inspection." The licensee documented this issue in CR 09-58004;
  • Unit 1: On May 6, 2009, inadvertent train 'A' safety injection signal was generated, while in mode 5, due to a faulty safety injection block switch.

Operators responded appropriately and no safety injection actually occurred.

Faulty switches were replaced. The licensee documented this issue in CR 09-58765; and

  • Unit 1 and Unit 2: On June 18, 2009, at 9:39 p.m., a dual-unit Unusual Event (UE) was declared in response to a fire alarm and CO2 system actuation in the Emergency Response Facility (ERF) substation. T he licensee entered emergency action level (EAL) 4.1. The onsite fire brigade responded and no fire was discovered, and determined there was a spurious actuation of the CO2 system. The UE was terminated at 10:36 p.m. The licensee is still investigating the cause, but is preliminarily attributed to a fire protection panel fault. The licensee documented this issue in CR 09-60763

.

b. Findings

No findings of significance were identified.

.2 Review of Licensee Event Reports (LERs) (1 sample)

(Closed) LER 05000334/2009-001-00: Surveillance Test Inadvertently Violates Technical Specification 3.6.1 for Containment Operability.

During a planned surveillance flow test on one of two outside re circulation spray system (RSS) pumps while in Mode 1, the suction and discharge containment isolation valves on the RSS train of piping were closed, but not de-energized. These valves receive an auto-open signal during a phase 'B' containment isolation. After the test, when the pump casing drain valve was opened to drain the system to restore to a normal configuration, the operations crew realized that the containment isolation valves needed to be de-energized in order to maintain containment operability. This condition existed in excess of seven hours, twice, during filling and draining sequences. This is contrary to the requirement in TS 3.6.1, "Containment". The crew immediately de-energized the affected valves.

The inspectors reviewed the LER, verified the appropriateness of corrective actions and extent of condition reviews, interviewed engineers and licensed operators, and completed a plant walkdown with FENOC engineers to identify the pump casing drain valve. Corrective actions include revising affected procedures to properly include TS 3.6.1. The enforcement aspects of the violation are discussed in Section 4OA7, Licensee Identified Violations. This LER is closed.

4OA5 Other Activities

.1 Quarterly Resident Inspector Observations of Security Personnel and Activities

a. Inspection Scope

During the inspection period, the inspectors conducted the following observations of security force personnel and activities to ensure that the activities were consistent with licensee security procedures and regulatory requirements relating to nuclear plant security. These observations took place during both normal and off-normal plant working hours. Specific examples include:

  • Observed operations within the central and secondary alarm stations;
  • Toured selected security towers and security officer response posts;
  • Observed security force shift turnover activities; and
  • Reviewed security logs and corrective action program documents which discussed security issues.

These quarterly resident inspector observations of security force personnel and activities did not constitute any additional inspection samples. Rather, they were considered an integral part of the inspectors' normal plant status review and inspection activities.

b. Findings

No findings of significance were identified.

.2 TI 2515/172, Reactor Coolant System Dissimilar Metal Butt Welds (Unit 1)

a. Inspection Scope

Temporary Instruction, TI 2515/172 provides for confirmation that owners of pressurized-water reactors (PWRs) have implemented the industry guidelines of the Materials Reliability Program (MRP) -

139 regarding nondestructive examination and evaluation of certain dissimilar metal (DM) welds in reactor coolant systems containing Alloy 600/82/182. The TI requires documentation of specific questions in an inspection report.

The questions and responses were previously documented in NRC Inspection Report 05000334, 412/2008003, Attachment B.

The hot and cold leg nozzle-to-safe end dissimilar metal (DM) welds of the "A" S/G were examined during this 1 st period inspection interval (1R19 outage). These welds were Risk-Informed ISI UT examined during 1R19. During the S/G replacement project 1R17, these particular nozzle welds were replaced with Alloy 52 and are resistant to stress-corrosion cracking and are considered Category "A" welds per MRP-139, Revision 1, and therefore the required examinations are per ASME Section XI. ASME Section XI, Table IWB-2500-1, B5.70 requires a volumetric and surface exam once per interval of the dissimilar metal welds for the S/G cold and hot leg nozzle-to-safe end welds. The Risk-Informed examination of these DM welds was only a UT examination (no surface exam) since these welds were selected in a particular piping segment per the Risk-Informed, ISI program that supersedes the ASME Section XI Code exam. The inspector reviewed the manual UT examination data records of the "A" S/G cold and hot leg nozzle-to-safe-end DM welds RC-E-1A-N11 and RC-E-1A-N12.

b. Findings

No findings of significance were identified.

4OA6 Meetings, Including Exit

.1 Access Control / ALARA Planning and Control

The inspector presented the inspection results of 2S01 and 2S02 to Mr. Kevin Ostrowski, Director of Site Operations, and other members of FENOC staff, at the conclusion of the inspection on April 30, 2009. No proprietary information is presented in this report.

.2 Inservice Inspection

The inspector presented the inspection results 1R08 to Mr. Kevin Ostrowski, Director of Site Operations, and other members of the FENOC staff at the conclusion of the ISI inspection at an exit meeting on May 7, 2009. Some proprietary information was reviewed during this inspection and was either returned or properly destroyed, but no proprietary information is presented in this report.

.3 Problem Identification and Resolution Submerged Cable Focus Sample

The inspectors presented the inspection results Mr. Peter Sena, Beaver Valley Site Vice President, and other members of FENOC staff, at the conclusion of the inspection on June 11, 2009. No proprietary information is presented in this report.

.4 Quarterly Exit Meeting Summary

On July 22, the inspectors presented the normal baseline inspection results to Mr. Ray Lieb, Director of Site Operations, and other members of the FENOC staff. The inspectors confirmed that proprietary information was not retained at the conclusion of the inspection period.

4OA7 Licensee-Identified Violations

The following violation of very low safety significance (Green) was identified by the licensee and is a violation of NRC requirements which meets the criteria of Section VI of the NRC Enforcement Policy, NUREG-1600, for being dispositioned as an NCV.

  • Technical Specification 3.6.1, "Containment," requires that containment operability be maintained in Mode 1, restored within one hour, or the reactor be shutdown to Mode 3 within six hours. Contrary to this requirement, FENOC failed

to maintain containment operability or restore cont ainment operability in the allowed time. Specifically, FENOC did not ensure containment isolation valves MOV-1RS-155B and MOV-1RS-156B were closed and de-energized prior to opening the 1RS-P-2B pump casing drain valve. The issue was entered into FENOC's corrective action program as CR 09-56250. The finding was more than minor because it is associated with the configuration control attribute of the barrier integrity cornerstone and affects the cornerstone objective of ensuring containment boundary preservation under postulated design-basis accident scenarios. The inspectors determined that the finding was of very low safety significance (Green), based on IMC 0609, Appendix H, Table 4.1 because this is a Type B finding and the affected pipe size is less than 2 inches in diameter.

ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee personnel

G. Alberti Steam Generator Program Owner

S. Baker Site, Radiation Protection Manager
R. Bologna Plant Engineering, Manager

T.Crella Senior Radiation Protection Technician

J. Fontaine Supervisor, ALARA

L. Freeland Director Performance Improvement

J. Freund Supervisor, Rad Operations Support
D. Girdwood Radiation Protection, Quality Assessor

D. Grabski ISI Coordinator

T. Heimel NDE Level III

W. Klinko, Diesel System Engineer

E. Lauck System Engineer

R. Lubert Electrical I&C/Plant Engineering, Supervisor

C. Miller Senior Radiation Protection Technician

J. Miller Site Fire Marshall

B. Murtagh Design, Supervisor
K. Ostrowski Director, Site Operations

J. Patterson RCS System Engineer

R. Pucci Senior Nuclear Specialist - ALARA

P. Sena Site Vice President

B. Sepelak Supervisor, Regulatory Compliance
D. Schwer Manager, Work Management

G. Storolis Unit 2 Shift Manager

J. Tweddell License Renewal

Other Personnel

D. Lew Director, Division of Reactor Projects, NRC Region I
R. Mathew Team Leader, NRC NRR
J. Rogge Branch Chief, NRC Region I
L. Ryan Inspector, Pennsylvania Department of Radiation Protection

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Open/Closed

05000334 / 2009003-01 NCV Inadequate Post-Maintenance Testing Specified for Safety-Related River Water Check Valve. (Section 1R19)
05000334, 412 / 2009003-02 NCV Continuously Submerged Cables Design Deficiency. (Section 4OA2.3)

Attachment

Closed

05000334 / 2009001-00 LER Surveillance test Inadvertently Violates Technical Specification 3.6.1 for Containment Operability. (Section
4OA3.2)

LIST OF DOCUMENTS REVIEWED

Section 1R01: Adverse Weather Protection

Procedures

1/2OM-53C.4A.35.1, Rev. 4, "Degraded Grid,"
NOP-OP-1003, Rev. 0, "Grid Reliability Pr otocol,"
NOP-OP-1007, Rev. 5, "Risk Determination,"

Condition Reports

09-60033 09-60106

Work Orders

200150639
200316056
200317926
200319210
200319961
200320671

Miscellaneous

BV-PA-09-02, Summer Readiness PMS not Completed by June 1st

Section 1R04: Equipment Alignment

Procedures

1DBD-24, Design Basis Document for Feedwater System
2OST-30.4, Service Water System A Header Valve Test
2DBD-30, Design Basis Document for Service Water System
2OM-30.4.D, Spare Service Water Pump Startup

Drawings

10080-RM-0411-001, Rev. 15, "Valve Oper No. Diagram Low/High Head Safety Injection
08700-RM-0436-001, Rev. 11, "Valve Oper No. Diagram Emergency Diesel Generator Air Start System" 8700-RM-0436-002, Rev. 9, "Valve Oper No. Diagram Emergency Diesel Gen. Fuel Oil System"
10080-RM-430-1, VOND Service Water Supply & Distribution
10080-RM-430-2, VOND Service Water Primary Cooling
10080-RM-430-3, VOND Service Water Primary Cooling
Attachment

Section 1R05: Fire Protection

Procedures

1OST-33.21, Containment Penetrations Area Fire Protection Test

Condition Reports

2-11507 08-49244 09-57425* 09-57811 09-60284 09-60911
09-60761 09-60762

Miscellaneous

Fire Protection Safe Shutdown Report; RTL# A1.080J, Addendum 28
RTL# A9.210X, Rev. 1
BVPS Unit 1 Appendix R Report, Chapter 11
BVPS Pre-Fire Plan for ERF Substation and ERF diesel generator building
BVPS Event Logs, dated June 18, 2009

Section 1R06: Flood Protection

Documents

reviewed are listed in section 4OA2 for this sample.

Section 1R08: Inservice Inspection

Procedures

NDE-VT-513, Visual Examination of the Reactor Vessel Bottom Mounted Instrumentation (BMI) Nozzles, Rev. 3
NDE-UT-323, Ultrasonic Examination of Welds Joining Cast Austenitic Piping Components, Rev. 2
ISIE-ECP-2, Steam Generator Examination Program, Rev. 21
1&2
ADM-2039, BVPS ISI Ten-Year Plans, Rev. 8
1&2
ADM-0801, ASME Section XI Repair/Replacement Program, Rev. 7
NOP-ER-2001, Boric Acid Corrosion Control Program, Rev. 7
Unit 1/2, NDE
GP-105, Evaluation of PSI/ISI Flaw Indications, Rev. 9 Unit 1/2,
ADM-2096, Alloy 600/690 Management Program, Rev. 7
PWSCC Susceptibility Assessment of the Alloy 600 and Alloy 82/182 Components in Beaver Valley Units 1 and 2, dated December 2003
NDE Examination Reports
UT-09-1009, 2" socket welded RCS drain line
RC-41-1502-Q1, completed 4/28/09
UT-09-1062,
RC-E-1A-N-11, Nozzle to safe-end DM weld (Hot Leg), completed 5/6/09
UT-09-1063,
RC-E-1A-N-12, Nozzle to safe-end DM weld (Cold Leg), completed 5/6/09
PT-09-1003,
RH-1-1-A-01 to 02, Welded attachment support
SH-40, completed 4/29/09
PT-09-1004,
RH-1-1-A-01 to 02, Welded attachment support
SH-40, completed 5/01/09
UT-09-1055,
DLW-LOOP3-7-S-02, RCS "C" loop cold leg pipe girth weld, completed 5/5/09
UT-09-1039, 1CNMT-Liner Area #3, completed 5/1/09
BOP-MT-09-029,
BV-1-RCBX, Primary Containment, Liner repair root pass, completed 5/4/09
BOP-MT-09-031,
BV-1-RCBX, Primary Containment, Liner plate final, completed 5/4/09
BOP-MT-09-032,
BV-1-RCBX, Primary Containment, Liner plate final, completed 5/4/09
BOP-UT-09-161, Containment liner repair plate butt weld, 45-degree scan, completed 5/4/09
BOP-UT-09-162, Containment liner repair plate butt weld, 60-degree scan, completed 5/4/09
BOP-VT-09-042,
VT-1, RBC Liner plate weld, completed 5/4/09
SG-CDME-07-24, BV Unit 1 Steam Generator Degradation Assessment 1R18 Refueling Outage, Rev.1
Attachment Work Orders
200367661
200366975
200367239
200367242

Condition Reports

07-25709 09-52089 09-54434 09-57589 09-57762 09-57665
09-57804 09-58004 09-58156

Section 1R12: Maintenance Rule Implementation

Procedures

1OST-15.1, Reactor Plant Component Cooling Water Pump Operating Surveillance Test

Condition Reports

07-27037 09-60127 09-59359

Section 1R13: Maintenance Risk Assessment and Emergent Work Control

Calculations

8700-DMC-1669, Rev. 1, Add. 1, "Time to RCS Boiling Calculation for the Pre-outage Shutdown Defense-in-Depth Report."

Procedures

NOP-OP-1007, Rev. 5, "Risk Determination"
1/2-ADM-2033, "Risk Management Program"

Work Orders

Condition Reports

09-57463 09-58491 09-58771 09-58775 09-58815
Other 1R19 Defense-In-Depth review for April 21, 2009
Unit 1 Weekly Maintenance Risk Summary for the week of June 15, Revs. 0 & 2
Unit 2 Weekly Maintenance Risk Summary for the week of June 15, Revs. 0 & 2

Section 1R15: Operability Evaluations

Calculations

8700-UR(B)-511
10080-UR(B)-510
241-UR(B)-427

Procedures

1OST-24.15B "Auxiliary Feedwater System Solid State Protection System Testing Train B"

Condition Reports

04-05251
06-01122
09-57966
09-58000
09-58798
09-59713
Attachment Miscellaneous Event Notification 45015, dated April 23, 2009
Engineering Change 09-0365-01, Repair Containment Liner Plate Hole
IN 2005-24
L-09-119, 10CFR 50.55a Request Number
BV1-IWE-2-2, dated April 28, 2009
Mode Hold Resolutions for 09-57589, 09-57762
NOTF
600538028,
600538316
NUREG-1522, Assessment of Inservice Conditions of Safety-Related Nuclear Plant Structures
RIS 2009-02, Rev. 1, "Use of Containment Atmosphere Gaseous Radioactivity Monitors for Reactor Coolant System Leakage Detection Equipment at Nuclear Power Reactors"
TSTF-513
WO 200124471,
200367013,
200367242
Unit 2 Fire Protection Safe Shutdown Report

Section 1R18: Plant Modifications

Condition Reports

09-57390
Regulatory Applicability Determination and 10
CFR 50.59 Screens
09-01453 09-0174

Procedures

1OM-52.4.R.1.F, Station Shutdown from 100% Power to Mode 5.

Drawings

8700-6.24-158 sheet1, Rev. 7
8700-6.24-158 sheet 8, Rev. 2
8700-6.24-158, sheet 9, Rev. 2
8700-RM-0430-001, Rev 30
8700-RM-407-1, Rev. 28
8700-2.19-0036, Rev. A

Work Orders

200359549
200359555
200313752
200313753

Miscellaneous

NUREG-0138,
NUREG-0224
EGG-EA-5826, TER Evaluation Report of the Overpressure protection System for the Beaver Valley Power Station Unit 1, dated March 1982.

Section 1R19: Post-Maintenance Testing

Procedures

1OST-36.2, Rev. 51, "Diesel Generator No. 2 Monthly Test"
1OM-36.4AN, Rev. 2, "Diesel Generator No. 2 Fast Start"

Work Orders

200124471
200308605
200284373
200296714
200296713
200367242
200369010
200233562
Attachment Condition Reports
09-57435 09-57813 09-58940
Miscellanous

Section 1R20: Refueling and Outage Activities

Procedures

1BVT-1.1.1, Rev. 4, "Rod Position Indication System Calibration Verification and Control Rod
Drop Test" 1BVT 2.1.1, Issue 1, Rev. 0, "Control Rod plant Exercise and Data Collection"
1OM-6.4.AO, Rev. 20, "Isolating and Draining a Reactor Coolant Loop"
1OM-20.4E, Rev. 31, "Draining The Refueling Cavity"
1OM-50.4D, Rev. 49, "Reactor Startup From Mode 3 to Mode 2"
1OM-50.4L, Rev. 18, "Plant Heatup From Mode 6 to Mode 3"
1OM-50.4L, Rev. 18, "Plant Heatup From Mode 6 to Mode 3, Data Sheet 2: RCS Heatup / Cooldown Determination" 1OM-52.4.K, Rev. 0, "Tavg Coastdown Operations"
1OM-52.4.R.1.F, Rev. 14, "Station Shutdown from 100% Power to Mode 5", Data Sheet 2: RCS Cooldown Determination Tables. 1OST-47.2B, Rev. 7, "Containment Closeout Inspection"
1OST-49.2, Rev. 22, "Shutdown Margin Calculation (Plant Shutdown) (Updated for Cycle 19)"
1MSP-9.04-M, Rev. 8, "Containment Sump Inspection"
1RP-3.2, Issue 0, Rev. 3, "Fuel Transfer System"
1RP-3.26, Rev. 7, "Refueling Procedure Upper Internals Assembly Installation"
1RP-3.28, Rev. 4, "Lower Internals Assembly Removal / Installation"
1RST-2.1, Rev. 11, "Initial Approach to Criticality After Refueling"
1RST-2.2, Rev. 10, "Core Design Check Test"
NOBP-OM-4010, Rev. 4, "Restart Readiness for Plant Outages"
NOBP-WM-5003, Rev. 1, "FENOC Rigging and Lifting Manual"
NOP-OP-1005, Rev. 10, "Shutdown Defense in Depth"
NOP-WM-5003, Rev. 1, "Rigging, Lifting, and Load Handling"

Drawings

8700-02.102-0050, Rev. A, "General Arrangement Transfer System" Cable Drive Installation, Transfer System - BVPS1, Rev. 1

Work Orders

Repetitive Task 10001 99-0201123-000
200285260
600426477

Miscellaneous

1R19 Outage Handbook Defense-In-Depth Report, 1R19, dated April 6, 2009 and updated May 16, 2009

Operating Experience

Handbook for BV 1R19
ECP 09-0035-001, BV1 and BV2 Tave / Power Coastdown, Master Package
8700-02.102-0010, UE&C Instruction Manual Cable Drive Fuel Transfer System
BVPS-1 Shift Operating / Refueling Logs dated April 19 - May 22, 2009
BV Unit 1 Cycle 20 Loading Pattern Map and Verification Video, reviewed May 12, 2009
NUREG-0612
Primavera Schedule, 1R19
Attachment Condition Reports
09-57474
09-57499
09-57762
09-57106
09-57589
09-59677
09-59702
09-60367
09-60572

Section 1R22: Surveillance Testing

Procedures

1OST-36.3, Train A EDG Autoload Test
1BVT-2.15.1, Rev. 5, " Reactor Plant Component Cooling Water Pumps [1CC-P-1A], [1CC-P-1B], [1CC-P-1C] Performance Curve Development"

Condition Reports

09-56250 09-57623 09-60127

Work Orders

& Notifications

WO 200309388
NOTF
600537878

Miscellaneous

Unit 1 Shift Operating Logs dated March 26 - 28, 2009
Sections 2OS1Access Control to Radiologically Significant Areas and
2OS2 ALARA Planning and Controls

Procedures

1/2-ADM-1601, Rev 15, Radiation Protection Standards
1/2-ADM-1611, Rev 9, Radiation Protection Administrative Guide
1/2-ADM-1621, Rev 3, ALARA Program
1/2-ADM-1630, Rev 10, Radiation Worker Practices
1/2-ADM-1631, Rev 5, Exposure Control
1/2-HPP-3.02.004, Rev 4, Area Posting
1/2-HPP-3.03.007, Rev 3, Transfer of Highly Radioactive Material from Plant Systems to Solid Waste 1/2-HPP-3.04.002, Rev 5, Bioassay Administration
1/2-HPP-3.05.001, Rev 4, Exposure Authorization
1/2-HPP-3.07.002, Rev 5, Radiation Survey Methods
1/2-HPP-3.07.013, Rev 3, Barrier Checks
1/2-HPP-3.08.001, Rev 8, Radiological Work Permit
1/2-HPP-3.08.003, Rev 10, Radiation Barrier Key Control
1/2-HPP-3.08.005, Rev 4, ALARA Review Program
1/2-HPP-3.08.006, Rev 1, Shielding
BVBP-RP-0003, Rev 4, Dosimetry Practices
BVBP-RP-0013, Rev 2, Radiation Protection Risk Assessment Process Attachment
BVBP-RP-0020, Rev 6, RP Job Coverage General Guidance
NOP-WM-7001, Rev 0, ALARA Program
NOP-WM-7002, Rev 0, Operational ALARA Program
NOP-WM-7003, Rev 0, Radiation Work Permit
NOP-WM-7017, Rev 0, Contamination Control Program
NOP-WM-7021, Rev 1, Radiological Postings, Labeling, and Markings
1/2-OM-18.4A.E, Rev 6, Removal of Spent Filter Cartridge From Filter Transfer Cask Nuclear Oversight Field Observation Reports Week of 4/20-26/2009

Condition Reports

09-58093 09-58195 09-58182 09-58115 09-58029 09-58162
09-58104 09-58043 09-58042 09-57896 09-57877 09-57843
09-57918 09-57701 09-57747 09-57797 09-57790 09-57810
09-57914 09-57901 09-55024 09-56516 09-56588 09-57570
09-57882
ALARA Plans & related Work-in-Progress /Post-Job Reviews
09-01-35, Permanent Scaffolding
09-01-33, Insulation Modifications (except Cavity Work)
09-01-25, Reactor Disassembly
09-01-41, Routine Valve Work
09-01-19, Replace/Dispose of Incore Detectors
09-01-24, Secondary Side Steam Generator Sludge Lancing/FOSAR
09-01-58, Flush/Change Resin
09-01-11, Changeout/Replace 1CH-FL-2 Filter
09-01-33, Insulation Removal/Replacement Modification
09-01-26, Remove/Replace Incore Detectors
09-01-29, In-Service Inspections
09-01-31, Scaffolding
ALARA Committee Meeting Minutes Meeting Nos. 09-01m/s, 09-02 m/s, 09-03 m/s, 09-04m/s, 09-05 m/s, 09-06 m, 09-07 m,
09-08 m, 09-09 m (m-manager's, s-subcommittee)

Miscellaneous

ALARA Reports
1R19 Outage ALARA Plan
EPRI Standard Radiation Monitoring Program - Unit 1 Source Term Measurements High Dose Individuals for 2009
Dose and Dose Rate Alarm Reports for 2009

Section 4OA2: Problem Identification and Resolution

Procedures

NORM-ER-3112, Rev. 1, Cable Monitoring
1/2-PMP-E-75-001, 4160 Rev. 8, VAC Motor Inspection and Lubrication
1/2-75-MANHOLE-1E, Rev. 4, Inspection of Manholes for Water Induced Damage Completed Procedures
1/2-PMP-E-75-001, 4160 VAC Motor Inspection and Lubrication, Rev. 8 dated 12/27/07
1/2-PMP-E-75-001, 4160 VAC Motor Inspection and Lubrication, Rev. 8 dated 02/08/08
Attachment 1/2-PMP-E-75-001, 4160 VAC Motor Inspection and Lubrication, Rev. 8 dated 08/15/08 1/2-PMP-E-75-001, 4160 VAC Motor Inspection and Lubrication, Rev. 8 dated 07/01/08
1/2-PMP-E-75-001, 4160 VAC Motor Inspection and Lubrication, Rev. 8 dated 05/19/08
1/2-PMP-E-75-001, 4160 VAC Motor Inspection and Lubrication, Rev. 8 dated 02/24/08
1/2-75-MANHOLE-1E, Inspection of Manholes for Water Induced Damage, Rev. 4 dated 09/26/06 1/2-75-MANHOLE-1E, Inspection of Manholes for Water Induced Damage, Rev. 4 dated 11/07/08
Miscellaneous:
BV UFSAR Unit 1, Rev. 20
Kerite Letter dated December 5, 1991
Kerite Letter dated February 18, 2009
GL 2007-01, Inaccessible of Underground Power Cable Failures That Disable Accident Mitigation Systems or Cause Plant Transients
IN 2002-12, Submerged Safety-Related Electrical Cables
IEEE 400.2, IEEE Guide for Field Testing of Shielded Power Cable Systems Using Very Low Frequency (VLF) Westinghouse Issue Report 08-124-M001
Condition Reports:
2-02302
2-02348
06-04144
06-06305
08-39693
08-42380
08-43594
09-60316
09-60387

Section 4OA3: Event Response

Condition Reports

09-57474
09-58477
09-58873
09-58900
09-58905
09-59155
09-60763
09-60768

Procedures

1/2-EPP-IP-1.1, Rev. 43, "Notifications", Att B. Unusual Event - Control Room
1/2-EPP-IP-1.2, Rev. 35, "Unusual Event"
1/2-EPP-IP-1.1.F01, Nuclear Power Plant Initial Notification Form, dated June 18, 2009
1OM-1.4.Z, Rev.0, "ESF Signal Reset By Alternate Method"
Attachment Work Orders
200366604
200306521
200366962
200366752
200351634
200306527
200390431
Event Notifications
45000, dated April 20, 2009
45001, dated April 20, 2009
45001 (retraction), dated May 12, 2009
45015, dated April 23, 2009
45022, dated April 26, 2009
45099, dated May 28, 2009
45143, dated June 18, 2009
Miscellaneous:
BV-SA-09-018, Snapshot Self-Assessment for Unit 1 Inadvertent SSPS Train A SI Signal on May 6, 2009 Mode Hold Resolutions for CRs 09-57499, 09-57474, 09-57762, 09-57589, 09-58004
NRC OpESS 2009-02, "Negative Trend and Recurring Events Involving Feedwater Systems" Shift Logs dated, June 18, 2009
Event Timeline, June 18, 2009

LIST OF ACRONYMS

ADM Administrative Procedure
ALARA As Low As is Reasonably Achievable
AP [[]]
ALARA Plan
ASME American Society of Mechanical Engineers
BACC Boric Acid Corrosion Control
BCO Basis for Continued Operations
BMI Bare Metal Inspection
BVPS Beaver Valley Power Station
CFR Code of Federal Regulations
CR Condition Report(s)
DM Dissimilar Metal
DPW Declared Pregnant Workers
EAL Emergency Action Level
ERF Emergency Response Facility
FA Functionality Assessments
FENOC First Energy Nuclear Operating Company
FOSAR Foreign Object Search and Retrieval
IOD Immediate Operability Determinations
IMC Inspection Manual Chapter
IP Inspection Procedure

ISI Inservice Inspection

LCO Limiting Conditions for Operations

Attachment

LER Licensee Event Report
LHRA Locked High Radiation Area
MR Maintenance Rule
MRP Materials Reliability Program
MSP Maintenance Surveillance Package
MT Magnetic Particle Testing
NDE Non-Destructive Examination
NRC Nuclear Regulatory Commission
NRR Nuclear Reactor Regulation
OD Operability Determinations
OST Operations Surveillance Test
PI Performance Indicator
PI&R Problem Identification and Resolution
PMT Post Maintenance Testing
POD Prompt Operability Determinations
PT Penetrant Testing
PWR Pressurized-Water Reactor
RBC Reactor Building Containment
RCS Reactor Coolant System
RHR Residual Heat Removal
RSS Recirculation Spray System
RWP Radiation Work Permit
SAC Station
ALARA Committee
SSC Structures, Systems, and Components
SG Steam Generator
TS Technical Specification
UE Unusual Event
UFSAR Updated Final Safety Analysis Report

UT Ultrasonic Testing

VT Visual Testing