IR 05000317/2004004: Difference between revisions

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{{IR-Nav| site = 05000317 | year = 2004 | report number = 004 | url = https://www.nrc.gov/reactors/operating/oversight/reports/calv_2004004.pdf }}
{{Adams
| number = ML041250174
| issue date = 04/30/2004
| title = IR 05000317-04-004 & 05000318-04-004, on 1/1/2004 Through 3/31/2004, for Calvert Cliffs Nuclear Plant, Units 1 and 2, Lusby, MD; Maintenance Effectiveness, Identification and Resolution of Problems
| author name = Trapp J
| author affiliation = NRC/RGN-I/DRP/PB1
| addressee name = Vanderheyden G
| addressee affiliation = Constellation Generation Group
| docket = 05000317, 05000318
| license number = DPR-053, DPR-069
| contact person =
| case reference number = EA-04-084
| document report number = IR-04-004
| document type = Inspection Report, Letter
| page count = 44
}}
 
{{IR-Nav| site = 05000317 | year = 2004 | report number = 004 }}
 
=Text=
{{#Wiki_filter:ril 30, 2004
 
==SUBJECT:==
CALVERT CLIFFS NUCLEAR POWER PLANT - NRC INTEGRATED INSPECTION REPORT 05000317/2004004 AND 05000318/2004004
 
==Dear Mr. Vanderheyden:==
On March 31, 2004, the US Nuclear Regulatory Commission (NRC) completed an inspection at your Calvert Cliffs Nuclear Power Plant Units 1 & 2. The enclosed report documents the inspection findings which were discussed on April 8, 2004, with members of your staff.
 
The inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license.
 
The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.
 
This report documents two self-revealing findings of very low safety significance (Green) which were determined to involve violations of NRC requirements. However, because of the very low safety significance and because the issue was entered into your corrective action program, the NRC is treating these findings as non-cited violations (NCV) consistent with Section VI.A of the NRC Enforcement Policy. Additionally, a licensee-identified violation, which was determined to be of very low safety significance is listed in this report. If you contest any NCV in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN. Document Control Desk, Washington, D.C. 20555-0001, with copies to the Regional Administrator, Region 1; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, D.C.
 
20555-0001; and the NRC Resident Inspector at the Calvert Cliffs Facility.
 
Since the terrorist attacks on September 11, 2001, the NRC has issued five Orders and several threat advisories to licensees of commercial power reactors to strengthen licensee capabilities, improve security force readiness, and enhance controls over access authorization. In addition to applicable baseline inspections, the NRC issued Temporary Instruction 2515/148, "Inspection of Nuclear Reactor Safeguards Interim Compensatory Measures," and its subsequent revision, to audit and inspect licensee implementation of the interim compensatory measures required by the order. Phase 1 of TI 2515/148 was completed at all commercial power nuclear power plants during calendar year 2002, and the remaining inspection activities for Calvert Cliffs were
 
Mr. George Vanderheyden  2 completed in July 2003. The NRC will continue to monitor overall safeguards and security controls at Calvert Cliffs.
 
In accordance with 10 CFR 2.390 of the NRCs "Rules of Practice," a copy of this letter and its enclosure and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRCs document system (ADAMS). ADAMS is accessible from the NRC Web Site at http://www.nrc.gov/reading-rm.html (the Public Electronic Reading Room).
 
Sincerely,
/RA/
James M. Trapp, Chief Projects Branch 1 Division of Reactor Projects Docket Nos.: 50-317, 50-318 License Nos.: DPR-53, DPR-69
 
===Enclosure:===
Inspection Report 05000317/2004004 and 05000318/2004004 w/Attachment: Supplemental Information
 
REGION I==
Docket Nos.: 50-317, 50-318 License Nos.: DPR-53, DPR-69 Report Nos.: 05000317/2004004 and 05000318/2004004 Licensee: Calvert Cliffs Nuclear Power Plant, Inc. (CCNPPI)
Facility: Calvert Cliffs Nuclear Power Plant Location: 1650 Calvert Cliffs Parkway Lusby, MD 20657-4702 Dates: January 1, 2004 - March 31, 2004 Inspectors: Mark A. Giles, Senior Resident Inspector Joseph M. OHara II, Resident Inspector John R. McFadden, Health Physicist Thomas Burns, Reactor Inspector Nancy McNamara, Emergency Preparedness Inspector Neil Perry, Senior Project Engineer Suresh Chaudhary, Reactor Inspector Approved by: James Trapp, Chief Projects Branch 1 Division of Reactor Projects ii  Enclosure
 
=SUMMARY OF FINDINGS=
IR 05000317/2004004, 05000318/2004004; 1/1/2004-3/31/2004; Calvert Cliffs Nuclear Plant,
 
Units 1 and 2; Maintenance Effectiveness, Identification and Resolution of Problems.
 
The report covered a three month period of inspection by resident inspectors and announced regional inspections including: an emergency preparedness inspector, a senior project engineer, two reactor inspectors, and a health physicist. The inspection identified two Green findings, which were determined to be non-cited violations. The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC)0609, "Significance Determination Process" (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.
 
===NRC-Identified and Self-Revealing Findings===
 
===Cornerstone: Mitigating Systems===
: '''Green.'''
The inspectors identified a non-cited violation of 10 CFR 50, Appendix B,
Criterion XVI, Corrective Actions, which requires that measures shall be established to assure significant conditions adverse to quality are promptly identified and corrected.
 
Specifically the licensee failed to promptly identify a significant condition adverse to quality associated with the #10 upper crankcase bearing on the 2A Emergency Diesel Generator (EDG). This condition if left uncorrected could have resulted in the failure of the EDG. This degraded condition occurred in 1995 and again in October 2003, on the 2A EDG. As a result of the October 2003 degraded condition, the licensee requested a Notice of Enforcement Discretion (NOED) since repair activities would exceed the allowable outage times as specified in Technical Specification (T.S.) 3.8.1, A.C.
 
Sources - Operating. The NRC granted an NOED to the licensee on October 10, 2003.
 
This finding is greater than minor because it affects the Reactor Safety, Mitigating Systems attribute of equipment performance, and the availability, reliability, and capability objective of the mitigating systems cornerstone. If left uncorrected, this condition could have led to the failure of the 2A EDG. This finding was of very low safety significance because the degraded condition did not result in an actual failure of the EDG to perform its safety function. The inspectors identified that a contributing cause of this finding was related to the cross-cutting area of Problem Identification and Resolution. (Section 1R12)
: '''Green.'''
The inspectors identified a non-cited violation of 10 CFR 50, Appendix B,
Criterion XVI, Corrective Actions, which requires that measures shall be established to assure significant conditions adverse to quality are promptly identified and corrected.
 
Specifically, the licensee failed to implement effective corrective actions for significant conditions adverse to quality associated with component mispositioning events. A similar failure was first identified as NCV 05000317; 05000318/2003009-01 and documented in NRC Inspection Report IR-2003-009, issued November 7, 2003. Since then, two additional significant component mispositioning events occurred between iv
 
Summary of Findings (contd)
October 29, 2003, and March 31, 2004 both resulting in actual consequences to safety-related systems.
 
This finding is greater than minor because it affects the Reactor Safety, Mitigating Systems attribute of human performance, and the availability, reliability, and capability objective of the mitigating systems cornerstone. This finding was of very low safety significance because none of the events resulted in the actual loss of a system safety function. The inspectors identified that a contributing cause of this finding was related to the cross-cutting area of Problem Identification and Resolution. (Section 4OA2)
 
===Licensee-Identified Violations===
 
One violation of very low safety significance, which was identified by the licensee, has been reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensees corrective action program. This violation is listed in Section 4OA7 of this report.
 
v
 
=REPORT DETAILS=
 
===Summary of Plant Status===
 
Unit 1 began the inspection period at 100 percent reactor power and remained unchanged until January 31, when power was reduced to about 67 percent for a brief period of time to support planned modifications on the 11 and 12 steam generator feedwater pump digital feedwater control systems. Following the modification, the unit remained at 100 percent reactor power until March 20, when a reactor trip occurred due to an induced ground which was caused during the performance of maintenance activities. Following repair activities, the unit was returned to 100 percent reactor power and remained there until March 30 when a rapid power reduction was performed to accommodate the potential impact from a fire protection system actuation.
 
The unit achieved 100 percent reactor power the following day and remained there the rest of the inspection period.
 
Unit 2 began the inspection period at 100 percent reactor power and remained there until a reactor trip occurred on January 23, due to the tripping of the 22 steam generator feedwater pump. The unit achieved 100 percent reactor power on January 25, and remained there until March 14, when power was reduced to about 68 percent to support the recovery of a dropped control element assembly. Following this recovery action, reactor power was increased to 100 percent and remained there until the inspection period ended.
 
==REACTOR SAFETY==
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity
{{a|1R04}}
==1R04 Equipment Alignment==
 
===1. Partial System Walkdown===
 
====a. Inspection Scope====
(71111.04Q - 3 samples)
The inspectors verified that select equipment trains of safety-related and risk significant systems were properly aligned. The inspectors reviewed plant documents to determine the correct system and power alignments, and the required positions of critical valves and breakers. The inspectors verified that the licensee had properly identified and resolved equipment alignment problems that could cause initiating events or potentially impact the availability of associated mitigating systems. The applicable documents for this inspection are located in the Attachment. The inspectors performed partial system walkdowns for the following systems:
* 12 Charging Pump (motor replacement)
* 23 Charging Pump (packing replacement and gearbox replacement)
* Chemical and Volume Control (2CVC-348 discharge drain valve replacement)
 
====b. Findings====
No findings of significance were identified.
 
===2. Complete System Walkdown (Semi-Annual)===
 
====a. Inspection Scope====
(71111.04S - 1 sample)
The inspectors conducted a complete walkdown of the risk significant salt water system.
 
The inspectors determined the correct system lineup using OI-29, Attachment 1, Saltwater System Valve Alignment, Attachment 2, Saltwater System Instrumentation Valve Alignment, and the appropriate piping and instrument drawings. Additionally, the inspectors reviewed outstanding design issues, temporary modifications, maintenance rule status, operator workarounds, and outstanding maintenance work requests and deficiencies that could affect the ability of the system to perform its functions. During the walkdown inspection, the inspectors verified the following: valves were correctly positioned and did not exhibit conditions which would impact their function; electrical power was available as required; labeling was correct; hangers and supports were correctly installed and functional; support systems were operational; valves required to be locked were properly locked; and there were no objects located such that they would interfere with system operation. Minor issues identified by the inspectors were provided to system engineering personnel.
 
====b. Findings====
No findings of significance were identified. {{a|1R05}}
==1R05 Fire Protection==
 
===1. Fire Brigade Observation (71111.05A - 2 samples)===
 
====a. Inspection Scope====
The inspectors observed a fire brigade drill conducted on February 27, 2004, involving a simulated fire in the Unit 2, 45 foot elevation west penetration room. The inspectors observed the brigade members donning protective equipment, transitioning to the scene of the fire, and fighting the simulated fire. The inspectors observed the fire brigade leader performing an assessment of the fire, communicating with team members and the control room supervisor, and directing the actions of the brigade to extinguish the fire. The inspectors attended the post drill debriefing between the assessment team and the fire brigade members. Constellation procedure SA-1-101, Fire Fighting, was referenced for this inspection activity.
 
On February 20, 2004 during a general plant tour, the inspectors noticed a small trash fire between a large dumpster full of combustible material and the loading dock behind the North Service Building. The inspectors reported the fire to the Unit 1 control room supervisor. In response, the plant fire alarm was sounded, and the fire brigade responded and quickly extinguished the fire with water. The area was raked clean of debris, and the dumpster was inspected to ensure the fire had not spread. Based on the possibility that the fire was started by an errant cigarette, the licensee posted the area as a non-smoking area.
 
====b. Findings====
No findings of significance were identified.
 
===2. Fire Area Walkdowns (71111.05Q - 7 samples)===
 
====a. Inspection Scope====
The inspectors walked down accessible portions of the plant to assess the licensees control of transient combustible material and ignition sources, fire detection and suppression capabilities, fire barriers, and any related compensatory measures. The inspectors assessed the material condition of fire protection suppression and detection equipment to determine whether any conditions or deficiencies existed which could impair the operability of that equipment. The inspectors reviewed administrative procedure SA-1-100, Fire Prevention, during the conduct of this inspection. The inspectors toured the following areas important to reactor safety:
* Unit 1 West Electrical Penetration Room
* Unit 1 East Electrical Penetration Room
* Unit 2 Component Cooling Water Pump Room
* Unit 1 Component Cooling Water Pump Room
* Unit 1 Turbine Auxiliary Feedwater Pump Room
* Unit 2, B Emergency Diesel Generator Room
* Unit 1, 11, 12, and 13 Charging Pump Room Area
 
====b. Findings====
No findings of significance were identified. {{a|1R07}}
==1R07 Heat Sink Performance (IP 71111.07B - 3 samples)==
 
====a. Inspection Scope====
The inspectors reviewed licensee programs and processes to ensure that the following system components could perform their design functions as intended:
* Shutdown cooling heat exchangers for both units
* Containment coolers for both units
* Station blackout and emergency diesel generator jacket water and lube oil coolers The shutdown cooling heat exchangers (HXs) are used to remove decay heat and reactor coolant sensible heat during plant cooldowns and cold shutdowns. The HXs also cool containment spray water during containment spray system operation. The shutdown cooling heat exchangers are cooled by the component cooling (CC) system.
 
The containment air recirculation and cooling system removes heat by circulating the post-accident containment atmosphere over coils cooled by the service water (SRW)system. The emergency diesel generator (EDG) jacket water and lube oil coolers are also cooled by SRW. The saltwater system provides the cooling medium for CC and SRW heat exchangers. The station blackout (SBO) diesel generator is cooled by a fan and radiator arrangement, and the jacket water cooling pump circulates engine coolant through the radiator tubes where engine heat is transferred to the outside air.
 
To ensure compatibility with commitments made in response to Generic Letter 89-13, Service Water System Problems Affecting Safety Related Equipment, the inspectors reviewed Constellations inspection, cleaning, and performance monitoring methods and frequency. The inspectors compared surveillance test and inspection data to the established acceptance criteria to verify that the results were acceptable and that operation was consistent with design.
 
Chemistry addition processes were reviewed for their effectiveness to ensure heat removal capabilities. The inspectors conducted interviews with knowledgeable personnel to assess challenges with various bio-fouling mechanisms. In addition, the inspectors walked down the SBO and Emergency Diesel Generator (1A and 2B) Rooms, the Unit 1 and Unit 2 CC heat exchangers, and the Unit 2 SRW heat exchangers to assess the material condition of these systems and components. The inspectors also observed maintenance and cleaning of the Unit 2 CC heat exchanger.
 
The inspectors also reviewed a sample of Issue Reports (IRs) related to the selected heat exchangers. This review was done to ensure that Constellation was appropriately identifying, characterizing, and correcting problems related to these components.
 
====b. Findings====
No findings of significance were identified.
 
{{a|1R11}}
==1R11 Licensed Operator Requalification Program==
{{IP sample|IP=IP 71111.11Q|count=1}}
 
====a. Inspection Scope====
The inspectors observed a licensed operator simulator training scenario conducted on March 9, 2004, in order to assess operator performance as well as operator requalification training. The scenario involved failures and operator challenges that operators encountered during the January 23, 2004 reactor trip event. These included:
the tripping of the 22 steam generator feed pump and its failure to reset which resulted in a reactor trip; an excessive steam demand event due to a failure of the turbine bypass valve/atmospheric dump valve quick open circuit; a pressurizer transient which required thermodynamic understanding and evaluation; and the failure of the safety injection actuation signal B train to reset. The inspection focused on high-risk operator actions performed during implementation of the emergency operating procedures, emergency plan implementation and classification, and the incorporation of lessons learned specific to the January 23, 2004, reactor trip event. The inspectors also evaluated the clarity and formality of communications, the implementation of appropriate actions in response to alarms, the performance of timely control board operation and manipulation, and the oversight and direction provided by the shift supervisor. The inspectors also reviewed simulator fidelity to evaluate the degree of similarity to the actual control room, especially regarding recent control board modifications.
 
====b. Findings====
No findings of significance were identified.
 
{{a|1R12}}
==1R12 Maintenance Effectiveness==
{{IP sample|IP=IP 71111.12Q|count=5}}
 
====a. Inspection Scope====
The inspectors reviewed the licensees effectiveness in performing routine maintenance activities. This review included an assessment of the licensees practices pertaining to the identification, scoping, and handling of degraded equipment conditions, as well as common cause failure evaluations and the resolution of historical equipment problems.
 
For those systems, structures, and components scoped in the maintenance rule per 10 CFR 50.65, the inspectors verified that reliability and unavailability were properly monitored and that 10 CFR 50.65 (a)(1) and (a)(2) classifications were justified in light of the reviewed degraded equipment condition. Documents applicable to this inspection are listed in the Attachment. The inspectors conducted this inspection for the following equipment issues:
* 2A EDG #10 Upper Crankcase Degraded Bearing
* 23 Charging Pump and Gearbox Overhaul
* Unit 2 Train B SIAS Failure To Reset
* 2B EDG Failed ERA Relay
* 12 Charging Pump Motor Replacement
 
====b. Findings====
 
=====Introduction:=====
A Green non-cited violation was identified for the licensees failure to comply with 10 CFR 50, Appendix B, Criterion XVI, Corrective Actions, specifically related to the licensees failure to perform an adequate root cause evaluation and effectively implement corrective actions associated with the degraded 2A EDG #10 upper crankcase bearing which was identified in 1995. As a result, this condition recurred in October 2003 during which the licensee requested a Notice of Enforcement Discretion (NOED) to support repair activities. During the repair, the licensee identified a distorted journal cap which not only caused the degraded bearing condition in October 2003, but was also the root cause of the degraded condition identified in 1995. The licensee failed to identify the distorted journal cap in 1995, when the opportunity existed, and improperly reinstalled the deformed part.
 
=====Description:=====
In March of 1994, the licensee performed a power uprate project on all three Fairbanks-Morse EDGs which increased the rated output from 2500 kW to 3000 kW. This project required a complete overhaul of the engine including the removal and reinstallation of the upper main crankshaft and the associated bearings and bearing journal caps. During the installation of the #10 upper main bearing and its associated bearing cap, the bearing cap was torqued down while improperly aligned. This was recognized because the bearing cap alignment dowel did not fit into the corresponding dowel hole in the upper bearing. Although this was corrected, and the installation was completed, the bearing cap was unknowingly distorted at that time.
 
On August 23, 1995, during a routine inspection of the 2A EDG, the licensee determined that the #10 upper crankcase bearing did not pass a standard feeler gage dimensional check and upon further inspection determined that the #10 upper bearing was degraded. The licensee conducted discussions with Fairbanks Morse technical representatives pertaining to the aspects of this degraded condition. As a result, the
#10 upper bearing was replaced. Measurements were taken during this replacement activity; however, no deficiencies were identified associated with the journal cap. The inspectors reviewed the licensees root cause that was performed at the time of this repair activity and determined that the root cause lacked sufficient rigor in that it failed to identify the root cause although the opportunity existed at that time. Following the maintenance activities, the 2A EDG was determined to be operable and returned to service.
 
On October 8, 2003, during the performance of a routine strainer inspection on the 2A EDG, aluminum particles were found in the suction strainer to the standby lube oil pump. The licensee discussed this condition with Fairbanks Morse representatives and determined that the aluminum particles were bearing material since the bearings were the only source of aluminum in the engine. The licensee performed visual inspections on the EDG and determined that the #10 upper crankcase bearing was again degraded, and required replacement. The licensee commenced a more extensive root cause evaluation to address this repetitive, degraded condition. During this evaluation, the licensee performed an additional dimensional check called a mandrel check that was not performed in 1995. This check identified that the #10 upper crankcase bearing journal cap was distorted. The inspectors reviewed the vendor technical manual in order to understand the troubleshooting guidance that was available in 1995, as well as in 2003, and also conducted discussions with engineering personnel to understand the licensees root cause determinations. Through this review, the inspectors noted that the mandrel check was identified in the appropriate section for troubleshooting bearing issues, and was incorporated in a 1984 vendor technical manual revision although the licensee utilized a 1970 revision during the 1995 troubleshooting and repair activities. The inspectors concluded that had the most current troubleshooting guidelines been utilized during the 1995 occurrence, the distorted journal cap could have reasonably been identified, and not reinstalled. In addition, during the review of the failure analysis report performed by Fairbanks Morse for the 1995 event, which was issued in 1998, the inspectors noted that the report indicated that the failure mechanism was due to improper installation of the bearing and journal cap in 1994. This conclusion was based on identified marks on the upper bearing half that were caused by the alignment dowel on the journal cap during installation. These marks were present during the 1995 repair activity yet did not lead the licensee to the identification of the distorted journal cap which existed at that time. Based on the above, the inspectors determined that the licensee failed to identify the distorted bearing cap in 1995 because the root cause which was performed at that time was inadequate.
 
=====Analysis:=====
The performance deficiency associated with this finding was that an adequate root cause evaluation, specific to the degraded bearing condition which existed in 1995, was not performed, and as such, the corrective actions were therefore not adequate to prevent recurrence as evidenced by the same degraded condition recurring in October 2003. Absent the performance of a comprehensive root cause evaluation including critical measurements of the journal cap in 1995, the inspectors concluded that the root cause of this recurring condition could have been determined in 1995, therefore preventing the degraded condition which recurred in 2003. This finding is greater than minor because it affects the Reactor Safety, Mitigating Systems attribute of equipment performance, and the availability, reliability, and capability objective of the mitigating systems cornerstone. If left uncorrected, the condition could have led to the failure of the 2A EDG. This issue was of very low safety significance (Green) because an actual EDG failure did not occur and no safety function was lost. Therefore, this issue screened out of the Phase 1 Reactor Safety SDP as a green finding.
 
=====Enforcement:=====
10 CFR 50, Appendix B, Criterion XVI, Corrective Actions, states, in part that measures shall be established to assure that significant conditions adverse to quality are promptly identified and corrected, and that the cause of the condition is determined and corrective actions are taken to preclude repetition. Contrary to the above, a significant condition adverse to quality involving the 2A EDG existed, and the licensee failed to identify the degraded condition and establish effective corrective actions to preclude repetition. Because this finding is of very low safety significance and has been entered into the licensees corrective action program as IR IR2003000375, this violation is being treated as an NCV, consistent with Section VI.A.1 of the NRC enforcement policy. EA-04-084; NCV 050000318/2004-04-01, Failure To Prevent Recurrence Of A Degraded Bearing Condition.
{{a|1R13}}
==1R13 Maintenance Risk Assessments and Emergent Work Evaluation (71111.13 - 5==
 
samples)
 
====a. Inspection Scope====
The inspectors reviewed the licensees assessments concerning the risk impact of removing from service those components associated with the work items listed below.
 
This review primarily focused on activities determined to be risk significant within the maintenance rule. The inspectors compared the risk assessments and risk management actions performed by station procedure NO-1-117, Integrated Risk Management, to the requirements of 10 CFR 50.65(a)(4), the recommendations of NUMARC 93-01, Revision 2, Industry Guideline for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants, Section 11, Evaluation of Systems to Be Removed From Service, and approved station procedures. The inspectors compared the assessed risk configurations to actual plant conditions to evaluate whether the assessments were accurate and comprehensive. In addition, the inspectors assessed the adequacy of the licensees identification and resolution of problems associated with maintenance risk assessments and emergent work activities. The inspectors reviewed the following selected work activities:
* 21 CCW Low Flow Switch Failure To Reset
* 23 Charging Pump Overhaul
* 2B EDG Relay Failure
* AFAS Channel ZF 21 S/G Hi/Low Level Alarm Relay Failure
* 13 PZR Heater Backup Breaker Failure of 480V Breaker to Close
 
====b. Findings====
No findings of significance were identified. {{a|1R14}}
==1R14 Operator Performance During Non-Routine Evolutions and Events==
{{IP sample|IP=IP 71111.14}}
 
===1. ===
===Unit 2 Reactor Trip (1 sample)===
On January 23, 2004, an automatic reactor trip occurred on Unit 2 from 100 percent reactor power. The inspectors responded to the control room to assess plant response and conditions specific to the event, and to evaluate the performance of licensed operators. The reactor trip was caused by the inadvertent tripping of the 22 steam generator feedwater pump which resulted in lowering steam generator levels resulting in an automatic reactor trip. The event was complicated by multiple equipment deficiencies and operator challenges which ultimately resulted in two safety injection actuations and the loss of the condenser as a secondary heat sink. The inspectors observed control room activities and the licensees use of emergency procedures while mitigating the event. The inspectors also reviewed control room recorder traces, databases containing information prior to and following the reactor trip, and graphs of critical primary and secondary parameters.
 
Based on the complicated nature of this trip, which involved multiple equipment malfunctions and potential operator performance deficiencies, the NRC established a Special Inspection Team (SIT) to perform detailed inspection of this event, and address potential deficiencies associated with the event. This inspection was initiated in accordance with NRC Inspection Procedure 71153 Event Follow-up, and NRC Management Directive 8.3, NRC Incident Investigation Program. The inspection will be conducted in accordance with NRC Inspection Procedure 93812, Special Inspection, and documented in NRC Inspection Report 2004-008.
 
===2. Unit 1 Reactor Trip (1 sample)===
 
On March 20, 2004, an automatic reactor trip occurred on Unit 1 from 100 percent reactor power. The inspectors responded to the control room in order to assess the event. The trip was uncomplicated with the exception that the Turbine Bypass Valves (TBV) did not function properly in auto or manual after the quick-open signal cleared.
 
While maintenance technicians were installing a 500 kv bus voltage recorder in control room panel 1C29 as part of preplanned maintenance, a wire was crimped between the recorder and the support railing. This induced a ground fault on non-vital instrument bus 1Y09. This condition lasted for several minutes and caused erratic and failed indications and controls associated with the digital feedwater system. The No. 11 steam generator feedwater pump (SGFP) feedwater regulating valve closed as a result of these control abnormalities, causing both SGFPs to trip on high discharge pressure.
 
The reactor automatically tripped on low SG level in the No. 11 steam generator (SG).
 
Other than the TBV problems, no significant malfunctions in plant equipment occurred that challenged the plant or control room operators. The licensee evaluated the extent of condition associated with the loads on 1Y09 to determine if additional degraded or failed components exist. The results of that inspection revealed no additional degraded components. The inspectors observed control room activities and procedures, and reviewed operator logs to determine if operators performed the appropriate actions in accordance with their training and established station procedures. The unit was restored to 100 percent reactor power on March 22, 2004. Further inspection regarding this event will be documented in NRC Special Inspection Report 2004-008.
 
===3. Unit 1 Rapid Downpower Due To An Actuation Of The Fire Protection System (1===
 
sample)
On March 30, 2004, a rapid downpower was performed on Unit 1 from 100 to 68 percent reactor power. This reduction in reactor power was performed in response to an unanticipated actuation of the fire protection system on the 27 foot elevation in the turbine building. This actuation occurred when ventilation was secured in an asbestos removal enclosure tent and temperatures exceeded the actuation point of a sprinkler head located within the enclosure. In order to preclude the possibility of a reactor trip due to the loss of a steam generator feed pump, the operators made a conservative decision to reduce power to a level that could withstand this loss without the initiation of a reactor trip. The inspectors were notified of this occurrence and responded to the site to assess plant conditions as well as to observe operator performance. The inspectors performed field walkdowns to evaluate the impact that the spray had on plant equipment located on the 27 foot and 12 foot turbine building elevations located underneath the enclosure area. The inspectors noted that some cable trays contained a small amount of water, however, this water was subsequently removed during the licensees cleanup efforts. The licensee took ground and voltage measurements that were satisfactory, inspected local motor control centers and breakers, and ensured that potentially affected equipment was working properly. In addition, the licensee confirmed that all equipment worked properly during the reduction in power. The inspectors confirmed by reviewing graphs, data, and documents that the licensee maintained reactor parameters within safe limits during the reduction in power. The unit was returned to 100 percent reactor power on March 31, 2004.
 
{{a|1R15}}
==1R15 Operability Evaluations==
{{IP sample|IP=IP 71111.15|count=5}}
 
====a. Inspection Scope====
The inspectors reviewed operability determinations to verify that the operability of systems important to safety was properly established, that the affected components or systems remained capable of performing their intended safety function, and that no unrecognized increase in plant or public risk occurred. In addition, the inspectors reviewed the selected operability determinations to verify they were performed in accordance with NO-1-106, Functional Evaluation - Operability Determination, and QL-2-100, Issue Reporting and Assessment. The inspectors reviewed the operability evaluations for the issues listed below which represented five inspection samples:
* 12 MSIV Excessive Oil Pressure
* 480 Volt Safety-Related Breakers Failures
* Emergency Diesel Generators With Failed ERA Relay
* Unit 1 CVCS Letdown Heat Exchanger Boric Acid Leak
* Unit 1 CVCS Unanalyzed Letdown Piping Support
 
====b. Findings====
No findings of significance were identified.
 
{{a|1R19}}
==1R19 Post-Maintenance Testing==
{{IP sample|IP=IP 71111.19|count=6}}
 
====a. Inspection Scope====
The inspectors observed and/or reviewed post-maintenance tests associated with the following work activities to verify that equipment was properly returned to service and that proper testing was specified and conducted to ensure that the equipment could perform its intended safety function, as described in the Updated Final Safety Analysis Report, following maintenance.
* 2A Emergency Diesel Generator Pressure Switch Replacement
* 2B Emergency Diesel Generator ERA Relay Replacement
* 1-CVC-504, RWT Charging Pump Suction Valve, Cleanup and Packing Check
* Unit 2 AFAS Channel ZF Power Supply Replacement
* Unit 1 ESFAS B LOCI Sequencer Replacement
* 1B Emergency Diesel Generator LOCI Sequencer Replacement
 
====b. Findings====
No findings of significance were identified.
 
{{a|1R22}}
==1R22 Surveillance Testing==
{{IP sample|IP=IP 71111.22|count=5}}
 
====a. Inspection Scope====
The inspectors observed and/or reviewed the five surveillance tests listed below associated with selected risk-significant systems, structures, and components (SSCs) to verify that technical specifications were properly complied with, and that test acceptance criteria were properly specified. The inspectors also verified that proper test conditions were established as specified in the procedures, that no equipment preconditioning activities occurred, and that acceptance criteria had been met.
* STP O-8B-1, Test Of 1B DG And 14 4KV Bus LOCI Sequencer
* STP O-5A-2, Auxiliary Feedwater System Quarterly Surveillance Test
* STP O-8B-2, Test Of 2B DG And 4 KV Bus 24 LOCI Sequencer
* STP O-73F-2, Boric Acid Pump Performance Test
* STP O-73D-1, Charging Pump Performance Test
 
====b. Findings====
No findings of significance were identified
{{a|1R23}}
==1R23 Temporary Plant Modifications==
{{IP sample|IP=IP 71111.23|count=5}}
 
====a. Inspection Scope====
The inspectors reviewed temporary modifications to determine whether system operability and availability were affected during and after the completion of the modifications. The inspectors verified that proper configuration control was maintained, appropriate operator briefings were planned, design modification packages were technically adequate, and post-installation testing was performed satisfactorily. The following inspection activities were reviewed against criteria in MD-1-100, Temporary Alterations.
* TMOD # 1-04-004 - Disable Trip Inputs From Digital Speed Monitor (DSM) on the Local Electronic Cabinets 1C194 (11 SGFPT)
* TMOD # 1-04-004 - Disable Trip Inputs From Digital Speed Monitor (DSM) on the Local Electronic Cabinets 1C195 (12 SGFPT)
* TMOD# 2-04-0004 - Remove Overspeed Trip Relay 2FTC21/OST from the SGFP 21 Speed Control
* TMOD# 2-04-0004 - Remove Overspeed Trip Relay 2FTC22/OST from the SGFP 22 Speed Control
* TMOD# 2-04-0006 - Remove Unit 2 SGFP Thrust Wear Trip Inputs
 
====b. Findings====
No findings of significance were identified.
 
===Cornerstone: Emergency Preparedness (EP)===
 
{{a|1EP4}}
==1EP4 Emergency Action Level (EAL) and Emergency Plan Changes==
{{IP sample|IP=IP 71114.04|count=1}}
 
====a. Inspection Scope====
A regional in-office review was conducted of licensee submitted revisions to the emergency plan, implementing procedures and EAL changes which were received by the NRC during the period of January - March 2004. A thorough review was conducted of aspects of the plan related to the risk significant planning standards (RSPS), such as classifications, notifications and protection action recommendations. A cursory review was conducted for non-RSPS portions. These changes were reviewed against 10 CFR 50.47(b) and the requirements of Appendix E. These changes are subject to future inspections to ensure that the impact of the changes continues to meet NRC regulations. The inspection was conducted in accordance with NRC Inspection Procedure 71114, Attachment 04, and the applicable requirements in 10 CFR 50.54(q)were used as reference criteria.
 
====b. Findings====
No findings of significance were identified.
 
{{a|1EP6}}
==1EP6 Drill Evaluation==
{{IP sample|IP=IP 71114.06|count=1}}
 
====a. Inspection Scope====
The inspectors observed a control room simulator training exercise conducted on March 9, 2004, to assess licensed operators performance in the area of emergency preparedness. This training exercise specifically focused on equipment failures and operator challenges that occurred during the Unit 2 reactor trip event on January 23, 2004, and the required procedural transitions and associated event classification. The observed scenario was performed in conjunction with the licensed operator requalification program. Details pertaining to this inspection are provided in Section 1R11 of this report.
 
====b. Findings====
No findings of significance were identified.
 
==RADIATION SAFETY==
 
===Cornerstone: Occupational Radiation Safety===
 
2OS1 Access Control to Radiologically Significant Areas (71121.01 - 3 samples)
 
====a. Inspection Scope====
The inspector reviewed radiological work activities and practices, and procedural implementation during observations and tours of the facilities, and inspected procedures, records and other program documents to evaluate the effectiveness of Calvert Cliffs access controls to radiologically significant areas. This inspection activity represents the completion of 3 samples relative to this inspection area (i.e., inspection procedure sections 02.03.a and 02.05.a and b) in partial fulfillment of the annual inspection requirements.
 
Problem Identification and Resolution (02.03.a)
During this week of inspection, the inspector reviewed the licensees self-assessment activities for any results related to the access control program since the last inspection.
 
The intent of this review was to determine if identified problems were entered into the corrective action program for resolution.
 
High Risk Significant, High Dose Rate HRA and VHRA Controls (02.05.a and b)
On February 2 through 5, the inspector met at various times with the Health Physics General Supervisor, the Health Physics Operations Supervisor, and the Health Physics Support Supervisor and discussed the controls and procedures for high-dose-rate high radiation areas (HRAs) and for very high radiation areas (VHRAs). The inspector reviewed the subject procedures (as listed in the List of Documents Reviewed section)to verify that the level of worker protection was adequate.
 
Related Activities On February 2 and 5, the inspector observed Radiologically-Controlled Area (RCA)entries and exits being made by radiation workers at the primary RCA access control point to verify compliance with requirements for RCA entry and exit, wearing of record dosimetry, and issuance and use of alarming electronic radiation dosimeters. The inspector toured various elevations in the auxiliary building to verify the adequacy of the radiological controls which were being implemented. The inspector reviewed observed work activities for compliance with the special work permit (SWP) requirements. During these observations and tours the inspector reviewed, for regulatory compliance, the posting, labeling, barricading, and level of radiological access control for locked high radiation areas (LHRAs), high radiation areas (HRAs), radiation and contamination areas, and radioactive material areas.
 
On February 4, the inspector examined the materials processing facility (MPF) and inspected the exteriors of locations used for radioactive material storage outside the protected area, including the independent spent fuel storage installation (ISFSI), the storage building for the old steam generators, and a large fenced storage area (Lake Davies).
 
On February 5, the inspector observed the morning turnover meetings for the Health Physics (HP) staff and for the HP technicians.
 
The inspector performed a selective examination of documents (as listed in the List of Documents Reviewed section) to evaluate the adequacy of radiological controls.
 
The review in this area was against criteria contained in 10 CFR 19.12, 10 CFR 20 (Subparts D, F, G, H, I, and J), Technical Specifications, and procedures.
 
====b. Findings====
No findings of significance were identified.
2OS2 ALARA Planning and Controls (71121.02 - 2 samples)
 
====a. Inspection Scope====
The inspector reviewed the effectiveness of the licensees program to maintain occupational radiation exposure as low as is reasonably achievable (ALARA). This inspection activity represents the completion of two
: (2) samples relative to this inspection area (i.e., inspection procedure sections 02.01.a and 02.03.a) in partial fulfillment of the annual inspection requirements.
 
Inspection Planning (02.01.a)
Prior to and during this inspection, the inspector reviewed pertinent information regarding plant collective exposure history, current exposure trends, and ongoing or planned activities in order to assess current performance and exposure challenges. The inspector determined the plants three-year rolling average collective exposure through the end of 2002. The inspector also reviewed the sites collective exposure for 2003.
 
Verification of Dose Estimates and Exposure Tracking Systems (02.03.a)
On February 3, at Warehouse 1, the inspector met with the Health Physics Work Leader (Radiological Engineering). During this meeting, the inspector reviewed the assumptions and basis for the current annual collective exposure estimate including that for the estimate for normal operations and that for the planned Unit 1 refueling outage.
 
The inspector also reviewed the applicable ALARA procedures used to determine the methodology for estimating work activity-specific exposures and the intended dose outcome.
 
Related Activities Issues, covered in the above-cited discussions, also included trends in on-line and outage exposures, outage SWPs, exposure tracking systems, the outage estimate breakdown, ALARA reviews, and the activities of the site ALARA committee.
 
Also, on February 3, at the Office Training Facility (OTF), the inspector met with the Health Physics Support Supervisor and discussed the HP high impact team (HIT) plan for the Unit 1 2004 refuel outage and the HP contingency plans, also for the Unit 1 2004 refuel outage.
 
On February 4, at Warehouse 1, the inspector observed a meeting of the HP HIT at which the 2004 refueling outage activity schedule for containment (April 9 through April 23, 2004) was reviewed.
 
The inspector performed a selective examination of documents (as listed in the List of Documents Reviewed section) for regulatory compliance and for adequacy of control of radiation exposure.
 
The review was against criteria contained in 10 CFR 20.1101 (Radiation protection programs), 10 CFR 20.1701 (Use of process or other engineering controls), and procedures.
 
====b. Findings====
No findings of significance were identified.
2OS3 Radiation Monitoring Instrumentation and Protective Equipment (71121.03 - 1 sample)
 
====a. Inspection Scope====
The inspector reviewed the program for health physics instrumentation to determine the accuracy and operability of the instrumentation. This inspection activity represents the completion of one
: (1) sample relative to this inspection area (i.e., inspection procedure section 02.04.b) in partial fulfillment of the annual inspection requirements.
 
Problem Identification and Resolution (02.04.b)
During this inspection, the inspector reviewed corrective action program reports related to incidents involving radiation monitoring instrument deficiencies since the last inspection in this area. The inspector interviewed the Health Physics Work Leader (Radiation Instruments) and discussed the reported radiation monitoring deficiencies and their resolution. The inspector also toured the radiation instrumentation calibration facilities in the South Service Building (SSB) and in the Office Training Facility (OTF).
 
The inspector performed a selective examination of documents (as listed in the List of Documents Reviewed section) for regulatory compliance and adequacy in this area.
 
The review was against criteria contained in 10 CFR 20.1501, 10 CFR 20 Subpart H, Technical Specifications, and procedures.
 
====b. Findings====
No findings of significance were identified.
 
==OTHER ACTIVITIES==
40A1 Performance Indicator Verification (71151)
During an EP program inspection conducted in July 2002 (50-317/02-010, 50-318/02-010), the inspector identified an Unresolved Item (URI 50-317/02-010-02, 50-318/02-010-02) regarding the licensees Alert and Notification System (ANS) PI data.
 
Specifically, due to operational problems because of an aging ANS, the licensee changed their testing methodology to perform three consecutive tests versus one during their weekly silent tests. They chose three tests because at a minimum, one of the three signals would result in a successful activation. However, when reporting the ANS PI data, the licensee considered the three silent tests as one test but was reporting successes on any of the three tests. The inspector determined that by not counting all the tests, the licensee could be unintentionally masking failures which may provide a false impression that the system was operating at a high performance level.
 
Constellation Generation Group believed the calculation of the data was correct because their testing method mimicked the signal activation of state-of-the-art systems currently being used by other power plants even though their system didnt operate in that manner. Constellation Generation Group submitted a Frequently Asked Question (FAQ) to the Nuclear Energy Institute (NEI) to determine if their interpretation of the guidance set forth in NEI 99-02, Revision 2 is correct and entered the issue in their corrective action system (No. IR3-021-087).
 
In November 2002, Constellation Generation Group presented their issue before the Reactor Oversight Process (ROP) Working Group Committee. In June 2003, the ROP Working Group Committee decided the issue would be reviewed generically (FAQ No.
 
35.7) with respect to whether a licensee is able to modify their ANS testing methodology for calculating the site ANS PI data. In February 2004 the FAQ was finalized which included a response specific to the Calvert Cliffs issue. The FAQ response stated it was not necessary for Constellation Generation Group to re-calculate their past PI data from the time of the change; however, the response directed the licensee to update the ANS PI data report by noting they had changed their testing method in the comment section which was submitted with their first quarter 2004 PI data report. Meanwhile, Constellation Nuclear Generation replaced their aging ANS in late 2003 with a newer system and changed their testing methodology back to counting each push as a test to accommodate the operability of the system. URI 50-317/02-010-02, 50-318/02-010-02 is considered closed.
 
{{a|4OA2}}
==4OA2 Identification and Resolution of Problems==
 
===1. Annual Sample Review===
 
====a. Inspection Scope====
The inspector selected seven issues identified in the Corrective Action Program (CAP)for detailed review (Issue Report Nos. IR4-008-987 and -988, IR4-009-607, -608, -642, and -680, and IR4-023-854). The issues were associated with site dose reduction, inadvertent release of radioactive material from the RCA, position qualifications, completion and documentation of required training, negative trends in written communications identified by self-assessment review, and documentation of radioactive material storage locations. On February 5, the inspector met with the Health Physics Support Supervisor to discuss these Issue Reports. The documented reports for the issues were reviewed to ensure that the full extent of the issues was identified, an appropriate evaluation was performed, and appropriate corrective actions were specified and prioritized.
 
====b. Findings====
No findings of significance were identified.
 
===2. Annual Sample Review===
 
====a. Inspection Scope====
( 1 sample)
The inspector selected Issue Report (IR) IR4-013-246 for detailed review. The IR identified a wall thinning condition downstream of flow orifice 1-FO-3710 in the Unit 1 reheat steam system. The wall thickness remaining was found to be degraded below specification requirements. This piping segment is scheduled for replacement during the refuel outage beginning April 2004, and, is currently restored to full pressure retaining capability by the installation of a mechanical clamp over the degraded area.
 
The IR was reviewed to ensure a complete and accurate identification of the issue, an appropriate root cause evaluation was performed, extent of condition was considered and corrective actions were specified and verified as completed. The IR and the resolution documents were reviewed against the requirements of Constellation Nuclears corrective action process. The inspector noted that during the review of extent-of-condition activities, the licensee replaced those piping segments downstream of the flow orifice on the remaining three moisture separator reheaters for Units 1 and 2.
 
The inspector noted that additional issue reports and a self assessment had been recently initiated related to the implementation of the Flow Accelerated Corrosion (FAC)
Program. Consequently, the inspector selected IR4-028-240, IR3-058-986, IR4-013-245, IR4-013-246 and Self Assessment 200200117 for review to assess the effectiveness of the FAC Program in meeting the requirements of NRC Bulletin 87-01 and Generic Letter 89-08 regarding the implementation of a Program to ensure that erosion/corrosion does not lead to degradation of single phase and two phase high-energy carbon steel systems.
 
The inspector also conducted interviews with personnel responsible for the implementation of the flow accelerated corrosion program to assess the effectiveness of the program to detect degraded pipe wall thickness in high energy applications.
 
====b. Findings====
No findings of significance were identified.
 
===3. Effectiveness Of Corrective Actions Associated With Mispositioning Events===
 
====a. Inspection Scope====
(1 sample)
The inspectors reviewed the licensees corrective action program documents pertaining to component mispositioning events. Including in these were issue reports, causal analysis reports, and previously implemented corrective actions. The inspectors also conducted interviews with various station personnel.
 
====b. Findings====
 
=====Introduction:=====
The inspectors identified a self-revealing finding of very low safety significance (Green) which resulted in a non-cited violation (NCV) for the licensees failure to establish adequate corrective actions associated with component mispositioning events as required by 10 CFR Part 50 Appendix B, Criterion XVI, Corrective Actions.
 
=====Description:=====
During the period of time between January 7, 2002 and March 31, 2004, there have been a total of fifty two component mispositioning events which were identified by the licensee and entered into their corrective action program. An NRC problem identification and resolution (PI&R) team inspection, which concluded on November 7, 2003, assessed 45 of these events which occurred between January 7, 2002, and October 28, 2003. This assessment resulted in the identification of a Green finding associated with the licensees failure to adequately establish and implement corrective actions to address the negative trend associated with component mispositionings [Inspection Report IR-2003-009, NCV 05000317; 05000318/2003009-01].
On October 29, 2003, the licensee issued IR4-016-119 to address this negative trend.
 
As a result, the licensee developed root causal analysis, IR200300402, which identified several underlying causes of the component mispositioning events. This analysis, dated December 23, 2003, provided a number of corrective actions designed to prevent the recurrence of mispositioning events.
 
Subsequent to these actions, the inspectors reviewed component mispositioning events that occurred between October 29, 2003, and March 31, 2004. These events represented seven of the fifty two events. Four of these events were classified as Category II IRs, which warranted a causal analysis; however, the inspectors determined that only two of these had risk significance. The first event occurred on March 4, 2004, during the performance of STP M-213-1, Calibration of Power Range Instrumentation by Comparison with Incore Nuclear Instrumentation. This STP was being performed on channel D of the Unit 1 Reactor Protection System. During the performance of this test, an instrumentation and controls technician inadvertently placed the channel C operate/test switch to zero. This resulted in a unintended trip condition on channel C, placing the system in a condition where a single failure in either the A or B channels could have resulted in a unit trip. The second event occurred on March 21, 2004, during the performance of OI-2A, Chemical & Volume Control System, Section 6.10, Purge and Establishment of Hydrogen Overpressure, when operators inadvertently closed valve 1-CVC-501, VCT Outlet Isolation. Although this valve was in a closed position for less than a minute, this action resulted in a loss of suction to all three charging pumps, causing the 12 charging pump to trip on low suction head, and causing the 13 charging pump to become gas bound. The 11 charging pump was not running at this time and was immediately available once suction was reestablished to the volume control tank (VCT). In light of these events, the inspectors determined that the licensees corrective actions to address component mispositioning thus far have not been fully effective in preventing component mispositioning events associated with risk significant components.
 
During the inspectors review of component mispositioning events, the inspectors noted an increase in tagout errors. Specifically, between October 29, 2003, and March 31, 2004, there were four tagout errors. Two of these were associated with safety-related systems, however, the inspectors determined that only one of these errors could have been potentially risk significant. This error involved a clearance order that intended to isolate the 22 service water (SRW) system by closing 2-SW-386, Manual SW Outlet.
 
The tagout incorrectly directed the closure of 2-SW-253, 21 A/B SRW Heat Exchanger Salt Water Outlet Isolation Valve. Had the tagout been performed as written, saltwater flow to both SRW subsystems would have been isolated, causing both subsystems to become inoperable. As field operators started closing 2-SW-253, 21 Saltwater Flow Trouble alarm was received in the control room. At the same time, field operators recognized changes in flow noises and stopped the tagout evolution, recognizing that the tagout was in error. The inspectors determined that this tagout error did not result in any adverse consequences to the plant, but considered the recent increase in tagout errors to be a contributor to the already identified negative trend of component mispositionings.
 
=====Analysis:=====
The inspectors determined that the ongoing adverse trend specifically associated with the safety-related component mispositioning events mentioned above constituted a significant condition adverse to quality, and that the licensees failure to take appropriate and timely corrective actions to resolve this negative trend constituted a performance deficiency. This finding is greater than minor because it affected the human performance attribute and the availability, reliability, and capability objectives of the mitigating system cornerstone.
 
The significance of this finding was evaluated in accordance with NRC Manual Chapter 0609, Appendix A, Attachment 1, Significance Determination Process (SDP) for Reactor Inspection Findings for At-Power Situations, and was determined to be of very low safety significance (Green) since none of the events resulted in the actual loss of a system safety function therefore, this issue screened out of the Phase I SDP as a Green finding.
 
=====Enforcement:=====
10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, states in part, that measures shall be established to assure that conditions adverse to quality are promptly identified and corrected; and for significant conditions adverse to quality, the measures shall assure that the cause of the condition is determined and corrective action taken to preclude recurrence. Contrary to the above, two significant conditions adverse to quality involving component mispositioning events associated with safety-related systems occurred between October 29, 2003, and March 31, 2004. These events are a continuance of a previously identified negative trend. The inspectors concluded that in light of the previously identified non-cited violation associated with component mispositioning events, prompt and effective corrective actions have not been adequately established to prevent the recurrence of similar events. Because these mispositioning events were of very low safety significance, and have been entered into the licensees corrective action program as IR4-030-128 and IR4-031-134 respectively, this violation is being treated as a non-cited violation (NCV), consistent with Section VI.A of the NRC Enforcement Policy. NCV 05000317; 05000318/2004-004-02, Failure To Implement Effective Corrective Actions Associated With Component Mispositioning Events.
 
===3. Cross-References to PI&R Findings Documented Elsewhere===
 
Section 1R12 describes a finding for failure to identify a degraded condition regarding a distorted journal cap on the 2A EDG. The licensee had an opportunity to identify the degraded condition in 1995.
 
{{a|4OA3}}
==4OA3 Event Follow-up (7 samples)==
 
===1. (Closed) Licensee Event Report (LER) 50-318/2003-01, Emergency Air Lock===
 
Containment Penetration Closure Requirements Violation On February 24, 2003, plant personnel identified a condition prohibited by technical specifications where a temporary hose penetrating the containment emergency air lock temporary closure device was not sealed, and core alterations had been ongoing.
 
Specifically, on February 23, core alterations (control element assembly uncoupling)were performed for approximately 8 hours and the containment emergency air lock temporary closure device was not closed (sealed) for approximately 5 of the 8 applicable hours, as required by technical specifications. The licensee determined the cause to be human error in that work packages were inadequate and there were inadequate communications. The work packages did not provide caution statements or adequately describe containment closure requirements necessary when performing work activities at the emergency air lock temporary closure device penetrations. The site procedure containing these cautions and closure requirements was not included in the work packages. Communications were inadequate in that the requirements for containment closure were not communicated or known to the individuals performing the task.
 
Corrective actions included changing plant procedures to require installation of chains and signs at the emergency air lock requiring notification of operations prior to entry and to require planners to include containment closure compliance steps in future work packages. This finding is more than minor because the finding is associated with the Barrier Integrity Cornerstone configuration control attribute and affected the cornerstone objective. The finding was considered to have very low safety significance (Green)using Appendix H of the SDP because the event did not occur within 8 days of the start of the outage. The inspector reviewed the procedure changes, and discussed the event and procedure changes with site personnel. This licensee-identified finding involved a violation of technical specifications and enforcement aspects of the violation are discussed in Section 4OA7. This LER is closed.
 
===2. (Closed) Licensee Event Report (LER) 50-318/2003-02, Unintentional Reactor===
 
Protective System (RPS) Actuation During Plant Heatup On April 19, 2003, during startup surveillance testing, while all control element assemblies were fully inserted into the core, Unit 2 received an automatic trip signal due to steam generator low pressure automatic bypass resetting prior to the trip signal reset.
 
Calvert Cliffs personnel determined that the cause for the event was a combination of setpoint tolerance, system design, and operating conditions. Corrective actions taken included revising related procedures to establish initial conditions such that tests cannot be conducted in the steam generator pressure range where this RPS actuation could occur, and evaluating all other RPS and Engineered Safety Features Actuation System trip inputs for similar unanticipated actuations resulting from configurations currently allowed by procedure. The inspector reviewed the procedure changes, and discussed the event and procedure changes with site personnel. The LER was reviewed by the inspectors and no findings of significance were identified. The licensee documented the event in Issue Report IR4-018-667. This LER is closed.
 
===3. (Closed) Licensee Event Report (LER) 50-318/2003-04-00 & 50-318/2003-04-01,===
 
Technical Specification Exceeded Due to Extended Repair of Diesel Generator On October 10, 2003, the licensee requested a Notice of Enforcement Discretion (NOED) due to the extended repair of the 2A EDG. The licensee determined the root cause of this event to be a human performance deficiency associated with the failure to identify a distorted journal cap in 1995 following an installation error of the journal cap and upper bearing in 1994. Details of this event are provided in Section 1R12 of this report. These LERs are closed.
 
===4. (Closed) Unresolved Item (URI) 50-318/2003-06-02, Review of Previous Maintenance===
 
and Vendor Related Activities Associated with the 2A EDG On October 10, 2003, the NRC granted a Unit 2 NOED related to enforcing compliance with the requirements of Technical Specification(TS) 3.8.1, AC Sources - Operating.
 
This was based on the licensees inability to perform repair activities on the 2A EDG #10 upper crankcase bearing within the established allowable outage time. The inspectors reviewed the applicable TS requirements, assessed the licensees inspection efforts pertaining to potential common-mode failure mechanisms affecting the other EDGs, and monitored compliance for granting of the NOED as well as the implemented compensatory actions during the extended outage duration.
 
Details pertaining to the dispositioning of this item are contained in Section 1R12 of this report. This URI is closed.
 
===5. Unit 2 Reactor Trip===
 
====a. Inspection Scope====
On January 23, 2004, the inspectors responded to the control room to assess plant conditions and operator performance following a Unit 2 reactor trip from 100 percent reactor power. This reactor trip was caused by the inadvertent tripping of the 22 steam generator feed pump which resulted in the lowering of steam generator levels below automatic reactor trip setpoints.
 
Based on the complicated nature of this trip, which involved multiple equipment malfunctions and operator performance deficiencies, the NRC established a Special Inspection Team (SIT) to perform detailed inspection of this event, and address potential deficiencies associated with the event. This inspection was initiated in accordance with NRC Inspection Procedure 71153 Event Follow-up, and NRC Management Directive 8.3, NRC Incident Investigation Program. The inspection will be conducted in accordance with NRC Inspection Procedure 93812, Special Inspection, and documented in NRC Inspection Report 2004-008.
 
====b. Findings====
No findings of significance were identified.
 
===6. Unit 1 Reactor Trip===
 
====a. Inspection Scope====
On March 20, 2004, the inspectors responded to the control room to assess maintenance activities that were in progress prior to a Unit 1 reactor trip, as well as plant conditions and operator performance following the event. The reactor trip occurred while at 100 percent reactor power. The trip was caused when maintenance activities induced a ground fault which resulted in erratic indications and failures associated with the digital feedwater system.
 
Based on the time that this event occurred, and in light of the ongoing NRC special inspection associated with the Unit 2 reactor trip mentioned above, the NRC determined to amend the original special inspection charter for the Unit 2 trip event, in order to appropriately assess related factors associated with this trip. Inspection results pertaining to this event will be documented in NRC Inspection Report 2004-008.
 
====b. Findings====
No findings of significance were identified.
 
===7. Rapid Downpower Due To Fire Protection System Actuation===
 
====a. Inspection Scope====
On March 30, 2004, the inspectors responded to the site to evaluate conditions leading up to and following a rapid downpower on Unit 1 from 100 percent to 68 percent reactor power. This downpower was performed as a conservative, anticipatory measure to preclude a potential reactor trip associated with the loss of a steam generator feedwater pump following the actuation of the fire protection system. A sprinkler head contained within an asbestos removal enclosure tent activated after exceeding its temperature setpoint and sprayed down cable trays in the vicinity of digital feedwater system control panels.
 
The inspectors reviewed station procedures to ensure compliance, performed walkdowns of the affected areas, and conducted discussions with engineering personnel to understand the circumstances that led to the actuation as well as the extent of condition prior to commencing a power increase. Further details pertaining to this event are provided in Section 1R14.
 
====b. Findings====
No findings of significance were identified.
{{a|4OA5}}
==4OA5 Other Activities==
 
Spent Fuel Material Control and Accounting at Nuclear Power Plants - Temporary Instruction 2515/154 Temporary Instruction 2515/154, Spent Fuel Material Control and Accounting at Nuclear Power Plants, Phase I and Phase II, were completed during this inspection period.
 
Appropriate documentation was provided to NRC management as required.
 
{{a|4OA6}}
==4OA6 Meetings, including Exit==
 
On April 8, 2004, the inspectors presented the inspection results to Kevin Neitmann and other members of his staff. The inspectors confirmed that proprietary information was not provided or examined during the inspection.
 
{{a|4OA7}}
==4OA7 Licensee-Identified Violations==
 
Technical Specification 3.9.3, Containment Penetrations, requires during core alterations, that the emergency air lock temporary closure device be closed. Contrary to this, on February 23, 2003, the closure device was not closed in that a hose penetrating the closure device was not sealed. This was identified in the corrective action program as IR4-015-307. This finding is of very low safety significance because it did not occur within 8 days of the start of the outage.
 
ATTACHMENT:
 
=SUPPLEMENTAL INFORMATION=
 
==KEY POINTS OF CONTACT==
 
===Licensee Personnel===
: [[contact::J. Ball]], Health Physics Work Leader, Radiological Engineering
: [[contact::S. Brown]], Health Physics Work Leader, Operations
Bill Carey, Operator
Keith Crissman, Electrical Maintenance
Sonny Dean, Auxiliary Systems Manager
Paul Fatka, System Manager
Dave Frye, Shift Manager
: [[contact::P. Furio]], Supervisor, Regulatory Matters
: [[contact::M. Geckle]], Operations Manager
: [[contact::J. Gines]], Mechanical Engineering Consultant
Chip Grooms, Shift Manager
: [[contact::J. Guidotti]], Health Physics Work Leader, Radiation Instruments
Calvin Hancock, Health Physics Supervisor
: [[contact::D. Holm]], Manager, Nuclear Maintenance
Mark Hunter, System Manager
: [[contact::S. Hutson]], Outage Management
: [[contact::J. Johnson]], Health Physics Technician
Al Kelly, Senior Reactor Operator
Keith King, Senior Reactor Operator
: [[contact::T. Kirkham]], Radiation Protection Supervisor
Joe Klecha, Operator
Ed Kreahling, System Manager
Hien Le, System Manager
: [[contact::J. Lenhart]], Health Physics Work Leader, Operations
Randy Lewis, Operator
: [[contact::S. Loeper]], mechanical Engineering Consultant
Dave Lynch, Shift Manager
Dale McElheny, System Manager
Roger McPherson, Operator
Homero Montes De Oca, Electrical Maintenance Supervisor
: [[contact::K. Neitmann]], Plant General Manager
Bob Pace, Shift Manager
: [[contact::B. Pickett]], Health Physics Technician
Tom Pilkerton, Mechanical Maintenance Supervisor
Mike Polak, Secondary Systems Manager
: [[contact::I. Rice]], Health Physics Technician
: [[contact::S. Sanders]], General Supervisor, Radiation Safety
Curtis Scayles, Mechanical Maintenance Supervisor
: [[contact::A. Simpson]], Regulatory Matters Supervisor
: [[contact::B. Scott]], Mechanical Engineering Consultant
: [[contact::G. Vanderheyden]], Vice President
Larry Vandersnick, Operator
Larry Williams, Systems Manager
: [[contact::J. York]], Health Physics Support Supervisor
: [[contact::M. Yox]], Engineering Analyst
 
==LIST OF ITEMS==
 
===OPENED, CLOSED AND DISCUSSED===
 
===Opened===
 
None
 
===Opened and Closed===
: 050000318/2004-04-01, EA-04-084 NCV        Failure To Prevent Recurrence Of A Degraded Bearing Condition (Section 1R12)
: 05000317;
: 05000318/2004-04-02      NCV    Failure To Implement Effective Corrective Actions Associated With Component Mispositioning Events (Section 4OA2)
50-318/2003-01                    LER    Emergency Air Lock Containment Penetration Closure Requirements Violation (Section 4OA3)
50-318/2003-02                    LER    Unintentional Reactor Protective System (RPS)
Actuation During Plant Heatup (Section 4OA3)
50-318/2003-04-00, 01              LER    Technical Specification Exceeded Due to Extended Repair of Diesel Generator (Section 4OA3)
 
===Closed===
 
50-317; 318/02-010-02              URI    ANS PI Data potentially not being calculated properly. (Section 4OA1)
50-318/2003-06-02                  URI    Review of Previous Maintenance and Vendor Related Activities Associated with the 2A EDG (Section 4OA3)
 
==LIST OF DOCUMENTS REVIEWED==
 
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Latest revision as of 05:13, 18 March 2020

IR 05000317-04-004 & 05000318-04-004, on 1/1/2004 Through 3/31/2004, for Calvert Cliffs Nuclear Plant, Units 1 and 2, Lusby, MD; Maintenance Effectiveness, Identification and Resolution of Problems
ML041250174
Person / Time
Site: Calvert Cliffs  Constellation icon.png
Issue date: 04/30/2004
From: James Trapp
Reactor Projects Branch 1
To: Vanderheyden G
Constellation Generation Group
References
EA-04-084 IR-04-004
Download: ML041250174 (44)


Text

ril 30, 2004

SUBJECT:

CALVERT CLIFFS NUCLEAR POWER PLANT - NRC INTEGRATED INSPECTION REPORT 05000317/2004004 AND 05000318/2004004

Dear Mr. Vanderheyden:

On March 31, 2004, the US Nuclear Regulatory Commission (NRC) completed an inspection at your Calvert Cliffs Nuclear Power Plant Units 1 & 2. The enclosed report documents the inspection findings which were discussed on April 8, 2004, with members of your staff.

The inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.

This report documents two self-revealing findings of very low safety significance (Green) which were determined to involve violations of NRC requirements. However, because of the very low safety significance and because the issue was entered into your corrective action program, the NRC is treating these findings as non-cited violations (NCV) consistent with Section VI.A of the NRC Enforcement Policy. Additionally, a licensee-identified violation, which was determined to be of very low safety significance is listed in this report. If you contest any NCV in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN. Document Control Desk, Washington, D.C. 20555-0001, with copies to the Regional Administrator, Region 1; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, D.C.

20555-0001; and the NRC Resident Inspector at the Calvert Cliffs Facility.

Since the terrorist attacks on September 11, 2001, the NRC has issued five Orders and several threat advisories to licensees of commercial power reactors to strengthen licensee capabilities, improve security force readiness, and enhance controls over access authorization. In addition to applicable baseline inspections, the NRC issued Temporary Instruction 2515/148, "Inspection of Nuclear Reactor Safeguards Interim Compensatory Measures," and its subsequent revision, to audit and inspect licensee implementation of the interim compensatory measures required by the order. Phase 1 of TI 2515/148 was completed at all commercial power nuclear power plants during calendar year 2002, and the remaining inspection activities for Calvert Cliffs were

Mr. George Vanderheyden 2 completed in July 2003. The NRC will continue to monitor overall safeguards and security controls at Calvert Cliffs.

In accordance with 10 CFR 2.390 of the NRCs "Rules of Practice," a copy of this letter and its enclosure and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRCs document system (ADAMS). ADAMS is accessible from the NRC Web Site at http://www.nrc.gov/reading-rm.html (the Public Electronic Reading Room).

Sincerely,

/RA/

James M. Trapp, Chief Projects Branch 1 Division of Reactor Projects Docket Nos.: 50-317, 50-318 License Nos.: DPR-53, DPR-69

Enclosure:

Inspection Report 05000317/2004004 and 05000318/2004004 w/Attachment: Supplemental Information

REGION I==

Docket Nos.: 50-317, 50-318 License Nos.: DPR-53, DPR-69 Report Nos.: 05000317/2004004 and 05000318/2004004 Licensee: Calvert Cliffs Nuclear Power Plant, Inc. (CCNPPI)

Facility: Calvert Cliffs Nuclear Power Plant Location: 1650 Calvert Cliffs Parkway Lusby, MD 20657-4702 Dates: January 1, 2004 - March 31, 2004 Inspectors: Mark A. Giles, Senior Resident Inspector Joseph M. OHara II, Resident Inspector John R. McFadden, Health Physicist Thomas Burns, Reactor Inspector Nancy McNamara, Emergency Preparedness Inspector Neil Perry, Senior Project Engineer Suresh Chaudhary, Reactor Inspector Approved by: James Trapp, Chief Projects Branch 1 Division of Reactor Projects ii Enclosure

SUMMARY OF FINDINGS

IR 05000317/2004004, 05000318/2004004; 1/1/2004-3/31/2004; Calvert Cliffs Nuclear Plant,

Units 1 and 2; Maintenance Effectiveness, Identification and Resolution of Problems.

The report covered a three month period of inspection by resident inspectors and announced regional inspections including: an emergency preparedness inspector, a senior project engineer, two reactor inspectors, and a health physicist. The inspection identified two Green findings, which were determined to be non-cited violations. The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC)0609, "Significance Determination Process" (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.

NRC-Identified and Self-Revealing Findings

Cornerstone: Mitigating Systems

Green.

The inspectors identified a non-cited violation of 10 CFR 50, Appendix B,

Criterion XVI, Corrective Actions, which requires that measures shall be established to assure significant conditions adverse to quality are promptly identified and corrected.

Specifically the licensee failed to promptly identify a significant condition adverse to quality associated with the #10 upper crankcase bearing on the 2A Emergency Diesel Generator (EDG). This condition if left uncorrected could have resulted in the failure of the EDG. This degraded condition occurred in 1995 and again in October 2003, on the 2A EDG. As a result of the October 2003 degraded condition, the licensee requested a Notice of Enforcement Discretion (NOED) since repair activities would exceed the allowable outage times as specified in Technical Specification (T.S.) 3.8.1, A.C.

Sources - Operating. The NRC granted an NOED to the licensee on October 10, 2003.

This finding is greater than minor because it affects the Reactor Safety, Mitigating Systems attribute of equipment performance, and the availability, reliability, and capability objective of the mitigating systems cornerstone. If left uncorrected, this condition could have led to the failure of the 2A EDG. This finding was of very low safety significance because the degraded condition did not result in an actual failure of the EDG to perform its safety function. The inspectors identified that a contributing cause of this finding was related to the cross-cutting area of Problem Identification and Resolution. (Section 1R12)

Green.

The inspectors identified a non-cited violation of 10 CFR 50, Appendix B,

Criterion XVI, Corrective Actions, which requires that measures shall be established to assure significant conditions adverse to quality are promptly identified and corrected.

Specifically, the licensee failed to implement effective corrective actions for significant conditions adverse to quality associated with component mispositioning events. A similar failure was first identified as NCV 05000317;05000318/2003009-01 and documented in NRC Inspection Report IR-2003-009, issued November 7, 2003. Since then, two additional significant component mispositioning events occurred between iv

Summary of Findings (contd)

October 29, 2003, and March 31, 2004 both resulting in actual consequences to safety-related systems.

This finding is greater than minor because it affects the Reactor Safety, Mitigating Systems attribute of human performance, and the availability, reliability, and capability objective of the mitigating systems cornerstone. This finding was of very low safety significance because none of the events resulted in the actual loss of a system safety function. The inspectors identified that a contributing cause of this finding was related to the cross-cutting area of Problem Identification and Resolution. (Section 4OA2)

Licensee-Identified Violations

One violation of very low safety significance, which was identified by the licensee, has been reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensees corrective action program. This violation is listed in Section 4OA7 of this report.

v

REPORT DETAILS

Summary of Plant Status

Unit 1 began the inspection period at 100 percent reactor power and remained unchanged until January 31, when power was reduced to about 67 percent for a brief period of time to support planned modifications on the 11 and 12 steam generator feedwater pump digital feedwater control systems. Following the modification, the unit remained at 100 percent reactor power until March 20, when a reactor trip occurred due to an induced ground which was caused during the performance of maintenance activities. Following repair activities, the unit was returned to 100 percent reactor power and remained there until March 30 when a rapid power reduction was performed to accommodate the potential impact from a fire protection system actuation.

The unit achieved 100 percent reactor power the following day and remained there the rest of the inspection period.

Unit 2 began the inspection period at 100 percent reactor power and remained there until a reactor trip occurred on January 23, due to the tripping of the 22 steam generator feedwater pump. The unit achieved 100 percent reactor power on January 25, and remained there until March 14, when power was reduced to about 68 percent to support the recovery of a dropped control element assembly. Following this recovery action, reactor power was increased to 100 percent and remained there until the inspection period ended.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity

1R04 Equipment Alignment

1. Partial System Walkdown

a. Inspection Scope

(71111.04Q - 3 samples)

The inspectors verified that select equipment trains of safety-related and risk significant systems were properly aligned. The inspectors reviewed plant documents to determine the correct system and power alignments, and the required positions of critical valves and breakers. The inspectors verified that the licensee had properly identified and resolved equipment alignment problems that could cause initiating events or potentially impact the availability of associated mitigating systems. The applicable documents for this inspection are located in the Attachment. The inspectors performed partial system walkdowns for the following systems:

  • 12 Charging Pump (motor replacement)
  • 23 Charging Pump (packing replacement and gearbox replacement)
  • Chemical and Volume Control (2CVC-348 discharge drain valve replacement)

b. Findings

No findings of significance were identified.

2. Complete System Walkdown (Semi-Annual)

a. Inspection Scope

(71111.04S - 1 sample)

The inspectors conducted a complete walkdown of the risk significant salt water system.

The inspectors determined the correct system lineup using OI-29, Attachment 1, Saltwater System Valve Alignment, Attachment 2, Saltwater System Instrumentation Valve Alignment, and the appropriate piping and instrument drawings. Additionally, the inspectors reviewed outstanding design issues, temporary modifications, maintenance rule status, operator workarounds, and outstanding maintenance work requests and deficiencies that could affect the ability of the system to perform its functions. During the walkdown inspection, the inspectors verified the following: valves were correctly positioned and did not exhibit conditions which would impact their function; electrical power was available as required; labeling was correct; hangers and supports were correctly installed and functional; support systems were operational; valves required to be locked were properly locked; and there were no objects located such that they would interfere with system operation. Minor issues identified by the inspectors were provided to system engineering personnel.

b. Findings

No findings of significance were identified.

1R05 Fire Protection

1. Fire Brigade Observation (71111.05A - 2 samples)

a. Inspection Scope

The inspectors observed a fire brigade drill conducted on February 27, 2004, involving a simulated fire in the Unit 2, 45 foot elevation west penetration room. The inspectors observed the brigade members donning protective equipment, transitioning to the scene of the fire, and fighting the simulated fire. The inspectors observed the fire brigade leader performing an assessment of the fire, communicating with team members and the control room supervisor, and directing the actions of the brigade to extinguish the fire. The inspectors attended the post drill debriefing between the assessment team and the fire brigade members. Constellation procedure SA-1-101, Fire Fighting, was referenced for this inspection activity.

On February 20, 2004 during a general plant tour, the inspectors noticed a small trash fire between a large dumpster full of combustible material and the loading dock behind the North Service Building. The inspectors reported the fire to the Unit 1 control room supervisor. In response, the plant fire alarm was sounded, and the fire brigade responded and quickly extinguished the fire with water. The area was raked clean of debris, and the dumpster was inspected to ensure the fire had not spread. Based on the possibility that the fire was started by an errant cigarette, the licensee posted the area as a non-smoking area.

b. Findings

No findings of significance were identified.

2. Fire Area Walkdowns (71111.05Q - 7 samples)

a. Inspection Scope

The inspectors walked down accessible portions of the plant to assess the licensees control of transient combustible material and ignition sources, fire detection and suppression capabilities, fire barriers, and any related compensatory measures. The inspectors assessed the material condition of fire protection suppression and detection equipment to determine whether any conditions or deficiencies existed which could impair the operability of that equipment. The inspectors reviewed administrative procedure SA-1-100, Fire Prevention, during the conduct of this inspection. The inspectors toured the following areas important to reactor safety:

  • Unit 1 West Electrical Penetration Room
  • Unit 1 East Electrical Penetration Room
  • Unit 2 Component Cooling Water Pump Room
  • Unit 1 Component Cooling Water Pump Room
  • Unit 1, 11, 12, and 13 Charging Pump Room Area

b. Findings

No findings of significance were identified.

1R07 Heat Sink Performance (IP 71111.07B - 3 samples)

a. Inspection Scope

The inspectors reviewed licensee programs and processes to ensure that the following system components could perform their design functions as intended:

  • Containment coolers for both units

The containment air recirculation and cooling system removes heat by circulating the post-accident containment atmosphere over coils cooled by the service water (SRW)system. The emergency diesel generator (EDG) jacket water and lube oil coolers are also cooled by SRW. The saltwater system provides the cooling medium for CC and SRW heat exchangers. The station blackout (SBO) diesel generator is cooled by a fan and radiator arrangement, and the jacket water cooling pump circulates engine coolant through the radiator tubes where engine heat is transferred to the outside air.

To ensure compatibility with commitments made in response to Generic Letter 89-13, Service Water System Problems Affecting Safety Related Equipment, the inspectors reviewed Constellations inspection, cleaning, and performance monitoring methods and frequency. The inspectors compared surveillance test and inspection data to the established acceptance criteria to verify that the results were acceptable and that operation was consistent with design.

Chemistry addition processes were reviewed for their effectiveness to ensure heat removal capabilities. The inspectors conducted interviews with knowledgeable personnel to assess challenges with various bio-fouling mechanisms. In addition, the inspectors walked down the SBO and Emergency Diesel Generator (1A and 2B) Rooms, the Unit 1 and Unit 2 CC heat exchangers, and the Unit 2 SRW heat exchangers to assess the material condition of these systems and components. The inspectors also observed maintenance and cleaning of the Unit 2 CC heat exchanger.

The inspectors also reviewed a sample of Issue Reports (IRs) related to the selected heat exchangers. This review was done to ensure that Constellation was appropriately identifying, characterizing, and correcting problems related to these components.

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification Program

a. Inspection Scope

The inspectors observed a licensed operator simulator training scenario conducted on March 9, 2004, in order to assess operator performance as well as operator requalification training. The scenario involved failures and operator challenges that operators encountered during the January 23, 2004 reactor trip event. These included:

the tripping of the 22 steam generator feed pump and its failure to reset which resulted in a reactor trip; an excessive steam demand event due to a failure of the turbine bypass valve/atmospheric dump valve quick open circuit; a pressurizer transient which required thermodynamic understanding and evaluation; and the failure of the safety injection actuation signal B train to reset. The inspection focused on high-risk operator actions performed during implementation of the emergency operating procedures, emergency plan implementation and classification, and the incorporation of lessons learned specific to the January 23, 2004, reactor trip event. The inspectors also evaluated the clarity and formality of communications, the implementation of appropriate actions in response to alarms, the performance of timely control board operation and manipulation, and the oversight and direction provided by the shift supervisor. The inspectors also reviewed simulator fidelity to evaluate the degree of similarity to the actual control room, especially regarding recent control board modifications.

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness

a. Inspection Scope

The inspectors reviewed the licensees effectiveness in performing routine maintenance activities. This review included an assessment of the licensees practices pertaining to the identification, scoping, and handling of degraded equipment conditions, as well as common cause failure evaluations and the resolution of historical equipment problems.

For those systems, structures, and components scoped in the maintenance rule per 10 CFR 50.65, the inspectors verified that reliability and unavailability were properly monitored and that 10 CFR 50.65 (a)(1) and (a)(2) classifications were justified in light of the reviewed degraded equipment condition. Documents applicable to this inspection are listed in the Attachment. The inspectors conducted this inspection for the following equipment issues:

  • 2A EDG #10 Upper Crankcase Degraded Bearing
  • 23 Charging Pump and Gearbox Overhaul
  • Unit 2 Train B SIAS Failure To Reset
  • 12 Charging Pump Motor Replacement

b. Findings

Introduction:

A Green non-cited violation was identified for the licensees failure to comply with 10 CFR 50, Appendix B, Criterion XVI, Corrective Actions, specifically related to the licensees failure to perform an adequate root cause evaluation and effectively implement corrective actions associated with the degraded 2A EDG #10 upper crankcase bearing which was identified in 1995. As a result, this condition recurred in October 2003 during which the licensee requested a Notice of Enforcement Discretion (NOED) to support repair activities. During the repair, the licensee identified a distorted journal cap which not only caused the degraded bearing condition in October 2003, but was also the root cause of the degraded condition identified in 1995. The licensee failed to identify the distorted journal cap in 1995, when the opportunity existed, and improperly reinstalled the deformed part.

Description:

In March of 1994, the licensee performed a power uprate project on all three Fairbanks-Morse EDGs which increased the rated output from 2500 kW to 3000 kW. This project required a complete overhaul of the engine including the removal and reinstallation of the upper main crankshaft and the associated bearings and bearing journal caps. During the installation of the #10 upper main bearing and its associated bearing cap, the bearing cap was torqued down while improperly aligned. This was recognized because the bearing cap alignment dowel did not fit into the corresponding dowel hole in the upper bearing. Although this was corrected, and the installation was completed, the bearing cap was unknowingly distorted at that time.

On August 23, 1995, during a routine inspection of the 2A EDG, the licensee determined that the #10 upper crankcase bearing did not pass a standard feeler gage dimensional check and upon further inspection determined that the #10 upper bearing was degraded. The licensee conducted discussions with Fairbanks Morse technical representatives pertaining to the aspects of this degraded condition. As a result, the

  1. 10 upper bearing was replaced. Measurements were taken during this replacement activity; however, no deficiencies were identified associated with the journal cap. The inspectors reviewed the licensees root cause that was performed at the time of this repair activity and determined that the root cause lacked sufficient rigor in that it failed to identify the root cause although the opportunity existed at that time. Following the maintenance activities, the 2A EDG was determined to be operable and returned to service.

On October 8, 2003, during the performance of a routine strainer inspection on the 2A EDG, aluminum particles were found in the suction strainer to the standby lube oil pump. The licensee discussed this condition with Fairbanks Morse representatives and determined that the aluminum particles were bearing material since the bearings were the only source of aluminum in the engine. The licensee performed visual inspections on the EDG and determined that the #10 upper crankcase bearing was again degraded, and required replacement. The licensee commenced a more extensive root cause evaluation to address this repetitive, degraded condition. During this evaluation, the licensee performed an additional dimensional check called a mandrel check that was not performed in 1995. This check identified that the #10 upper crankcase bearing journal cap was distorted. The inspectors reviewed the vendor technical manual in order to understand the troubleshooting guidance that was available in 1995, as well as in 2003, and also conducted discussions with engineering personnel to understand the licensees root cause determinations. Through this review, the inspectors noted that the mandrel check was identified in the appropriate section for troubleshooting bearing issues, and was incorporated in a 1984 vendor technical manual revision although the licensee utilized a 1970 revision during the 1995 troubleshooting and repair activities. The inspectors concluded that had the most current troubleshooting guidelines been utilized during the 1995 occurrence, the distorted journal cap could have reasonably been identified, and not reinstalled. In addition, during the review of the failure analysis report performed by Fairbanks Morse for the 1995 event, which was issued in 1998, the inspectors noted that the report indicated that the failure mechanism was due to improper installation of the bearing and journal cap in 1994. This conclusion was based on identified marks on the upper bearing half that were caused by the alignment dowel on the journal cap during installation. These marks were present during the 1995 repair activity yet did not lead the licensee to the identification of the distorted journal cap which existed at that time. Based on the above, the inspectors determined that the licensee failed to identify the distorted bearing cap in 1995 because the root cause which was performed at that time was inadequate.

Analysis:

The performance deficiency associated with this finding was that an adequate root cause evaluation, specific to the degraded bearing condition which existed in 1995, was not performed, and as such, the corrective actions were therefore not adequate to prevent recurrence as evidenced by the same degraded condition recurring in October 2003. Absent the performance of a comprehensive root cause evaluation including critical measurements of the journal cap in 1995, the inspectors concluded that the root cause of this recurring condition could have been determined in 1995, therefore preventing the degraded condition which recurred in 2003. This finding is greater than minor because it affects the Reactor Safety, Mitigating Systems attribute of equipment performance, and the availability, reliability, and capability objective of the mitigating systems cornerstone. If left uncorrected, the condition could have led to the failure of the 2A EDG. This issue was of very low safety significance (Green) because an actual EDG failure did not occur and no safety function was lost. Therefore, this issue screened out of the Phase 1 Reactor Safety SDP as a green finding.

Enforcement:

10 CFR 50, Appendix B, Criterion XVI, Corrective Actions, states, in part that measures shall be established to assure that significant conditions adverse to quality are promptly identified and corrected, and that the cause of the condition is determined and corrective actions are taken to preclude repetition. Contrary to the above, a significant condition adverse to quality involving the 2A EDG existed, and the licensee failed to identify the degraded condition and establish effective corrective actions to preclude repetition. Because this finding is of very low safety significance and has been entered into the licensees corrective action program as IR IR2003000375, this violation is being treated as an NCV, consistent with Section VI.A.1 of the NRC enforcement policy. EA-04-084; NCV 050000318/2004-04-01, Failure To Prevent Recurrence Of A Degraded Bearing Condition.

1R13 Maintenance Risk Assessments and Emergent Work Evaluation (71111.13 - 5

samples)

a. Inspection Scope

The inspectors reviewed the licensees assessments concerning the risk impact of removing from service those components associated with the work items listed below.

This review primarily focused on activities determined to be risk significant within the maintenance rule. The inspectors compared the risk assessments and risk management actions performed by station procedure NO-1-117, Integrated Risk Management, to the requirements of 10 CFR 50.65(a)(4), the recommendations of NUMARC 93-01, Revision 2, Industry Guideline for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants, Section 11, Evaluation of Systems to Be Removed From Service, and approved station procedures. The inspectors compared the assessed risk configurations to actual plant conditions to evaluate whether the assessments were accurate and comprehensive. In addition, the inspectors assessed the adequacy of the licensees identification and resolution of problems associated with maintenance risk assessments and emergent work activities. The inspectors reviewed the following selected work activities:

  • 21 CCW Low Flow Switch Failure To Reset
  • 23 Charging Pump Overhaul
  • 2B EDG Relay Failure
  • AFAS Channel ZF 21 S/G Hi/Low Level Alarm Relay Failure
  • 13 PZR Heater Backup Breaker Failure of 480V Breaker to Close

b. Findings

No findings of significance were identified.

1R14 Operator Performance During Non-Routine Evolutions and Events

1.

Unit 2 Reactor Trip (1 sample)

On January 23, 2004, an automatic reactor trip occurred on Unit 2 from 100 percent reactor power. The inspectors responded to the control room to assess plant response and conditions specific to the event, and to evaluate the performance of licensed operators. The reactor trip was caused by the inadvertent tripping of the 22 steam generator feedwater pump which resulted in lowering steam generator levels resulting in an automatic reactor trip. The event was complicated by multiple equipment deficiencies and operator challenges which ultimately resulted in two safety injection actuations and the loss of the condenser as a secondary heat sink. The inspectors observed control room activities and the licensees use of emergency procedures while mitigating the event. The inspectors also reviewed control room recorder traces, databases containing information prior to and following the reactor trip, and graphs of critical primary and secondary parameters.

Based on the complicated nature of this trip, which involved multiple equipment malfunctions and potential operator performance deficiencies, the NRC established a Special Inspection Team (SIT) to perform detailed inspection of this event, and address potential deficiencies associated with the event. This inspection was initiated in accordance with NRC Inspection Procedure 71153 Event Follow-up, and NRC Management Directive 8.3, NRC Incident Investigation Program. The inspection will be conducted in accordance with NRC Inspection Procedure 93812, Special Inspection, and documented in NRC Inspection Report 2004-008.

2. Unit 1 Reactor Trip (1 sample)

On March 20, 2004, an automatic reactor trip occurred on Unit 1 from 100 percent reactor power. The inspectors responded to the control room in order to assess the event. The trip was uncomplicated with the exception that the Turbine Bypass Valves (TBV) did not function properly in auto or manual after the quick-open signal cleared.

While maintenance technicians were installing a 500 kv bus voltage recorder in control room panel 1C29 as part of preplanned maintenance, a wire was crimped between the recorder and the support railing. This induced a ground fault on non-vital instrument bus 1Y09. This condition lasted for several minutes and caused erratic and failed indications and controls associated with the digital feedwater system. The No. 11 steam generator feedwater pump (SGFP) feedwater regulating valve closed as a result of these control abnormalities, causing both SGFPs to trip on high discharge pressure.

The reactor automatically tripped on low SG level in the No. 11 steam generator (SG).

Other than the TBV problems, no significant malfunctions in plant equipment occurred that challenged the plant or control room operators. The licensee evaluated the extent of condition associated with the loads on 1Y09 to determine if additional degraded or failed components exist. The results of that inspection revealed no additional degraded components. The inspectors observed control room activities and procedures, and reviewed operator logs to determine if operators performed the appropriate actions in accordance with their training and established station procedures. The unit was restored to 100 percent reactor power on March 22, 2004. Further inspection regarding this event will be documented in NRC Special Inspection Report 2004-008.

3. Unit 1 Rapid Downpower Due To An Actuation Of The Fire Protection System (1

sample)

On March 30, 2004, a rapid downpower was performed on Unit 1 from 100 to 68 percent reactor power. This reduction in reactor power was performed in response to an unanticipated actuation of the fire protection system on the 27 foot elevation in the turbine building. This actuation occurred when ventilation was secured in an asbestos removal enclosure tent and temperatures exceeded the actuation point of a sprinkler head located within the enclosure. In order to preclude the possibility of a reactor trip due to the loss of a steam generator feed pump, the operators made a conservative decision to reduce power to a level that could withstand this loss without the initiation of a reactor trip. The inspectors were notified of this occurrence and responded to the site to assess plant conditions as well as to observe operator performance. The inspectors performed field walkdowns to evaluate the impact that the spray had on plant equipment located on the 27 foot and 12 foot turbine building elevations located underneath the enclosure area. The inspectors noted that some cable trays contained a small amount of water, however, this water was subsequently removed during the licensees cleanup efforts. The licensee took ground and voltage measurements that were satisfactory, inspected local motor control centers and breakers, and ensured that potentially affected equipment was working properly. In addition, the licensee confirmed that all equipment worked properly during the reduction in power. The inspectors confirmed by reviewing graphs, data, and documents that the licensee maintained reactor parameters within safe limits during the reduction in power. The unit was returned to 100 percent reactor power on March 31, 2004.

1R15 Operability Evaluations

a. Inspection Scope

The inspectors reviewed operability determinations to verify that the operability of systems important to safety was properly established, that the affected components or systems remained capable of performing their intended safety function, and that no unrecognized increase in plant or public risk occurred. In addition, the inspectors reviewed the selected operability determinations to verify they were performed in accordance with NO-1-106, Functional Evaluation - Operability Determination, and QL-2-100, Issue Reporting and Assessment. The inspectors reviewed the operability evaluations for the issues listed below which represented five inspection samples:

  • 12 MSIV Excessive Oil Pressure
  • 480 Volt Safety-Related Breakers Failures
  • Unit 1 CVCS Unanalyzed Letdown Piping Support

b. Findings

No findings of significance were identified.

1R19 Post-Maintenance Testing

a. Inspection Scope

The inspectors observed and/or reviewed post-maintenance tests associated with the following work activities to verify that equipment was properly returned to service and that proper testing was specified and conducted to ensure that the equipment could perform its intended safety function, as described in the Updated Final Safety Analysis Report, following maintenance.

  • 1-CVC-504, RWT Charging Pump Suction Valve, Cleanup and Packing Check
  • Unit 2 AFAS Channel ZF Power Supply Replacement
  • Unit 1 ESFAS B LOCI Sequencer Replacement

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing

a. Inspection Scope

The inspectors observed and/or reviewed the five surveillance tests listed below associated with selected risk-significant systems, structures, and components (SSCs) to verify that technical specifications were properly complied with, and that test acceptance criteria were properly specified. The inspectors also verified that proper test conditions were established as specified in the procedures, that no equipment preconditioning activities occurred, and that acceptance criteria had been met.

  • STP O-8B-1, Test Of 1B DG And 14 4KV Bus LOCI Sequencer
  • STP O-8B-2, Test Of 2B DG And 4 KV Bus 24 LOCI Sequencer
  • STP O-73D-1, Charging Pump Performance Test

b. Findings

No findings of significance were identified

1R23 Temporary Plant Modifications

a. Inspection Scope

The inspectors reviewed temporary modifications to determine whether system operability and availability were affected during and after the completion of the modifications. The inspectors verified that proper configuration control was maintained, appropriate operator briefings were planned, design modification packages were technically adequate, and post-installation testing was performed satisfactorily. The following inspection activities were reviewed against criteria in MD-1-100, Temporary Alterations.

  • TMOD # 1-04-004 - Disable Trip Inputs From Digital Speed Monitor (DSM) on the Local Electronic Cabinets 1C194 (11 SGFPT)
  • TMOD # 1-04-004 - Disable Trip Inputs From Digital Speed Monitor (DSM) on the Local Electronic Cabinets 1C195 (12 SGFPT)
  • TMOD# 2-04-0004 - Remove Overspeed Trip Relay 2FTC21/OST from the SGFP 21 Speed Control
  • TMOD# 2-04-0004 - Remove Overspeed Trip Relay 2FTC22/OST from the SGFP 22 Speed Control
  • TMOD# 2-04-0006 - Remove Unit 2 SGFP Thrust Wear Trip Inputs

b. Findings

No findings of significance were identified.

Cornerstone: Emergency Preparedness (EP)

1EP4 Emergency Action Level (EAL) and Emergency Plan Changes

a. Inspection Scope

A regional in-office review was conducted of licensee submitted revisions to the emergency plan, implementing procedures and EAL changes which were received by the NRC during the period of January - March 2004. A thorough review was conducted of aspects of the plan related to the risk significant planning standards (RSPS), such as classifications, notifications and protection action recommendations. A cursory review was conducted for non-RSPS portions. These changes were reviewed against 10 CFR 50.47(b) and the requirements of Appendix E. These changes are subject to future inspections to ensure that the impact of the changes continues to meet NRC regulations. The inspection was conducted in accordance with NRC Inspection Procedure 71114, Attachment 04, and the applicable requirements in 10 CFR 50.54(q)were used as reference criteria.

b. Findings

No findings of significance were identified.

1EP6 Drill Evaluation

a. Inspection Scope

The inspectors observed a control room simulator training exercise conducted on March 9, 2004, to assess licensed operators performance in the area of emergency preparedness. This training exercise specifically focused on equipment failures and operator challenges that occurred during the Unit 2 reactor trip event on January 23, 2004, and the required procedural transitions and associated event classification. The observed scenario was performed in conjunction with the licensed operator requalification program. Details pertaining to this inspection are provided in Section 1R11 of this report.

b. Findings

No findings of significance were identified.

RADIATION SAFETY

Cornerstone: Occupational Radiation Safety

2OS1 Access Control to Radiologically Significant Areas (71121.01 - 3 samples)

a. Inspection Scope

The inspector reviewed radiological work activities and practices, and procedural implementation during observations and tours of the facilities, and inspected procedures, records and other program documents to evaluate the effectiveness of Calvert Cliffs access controls to radiologically significant areas. This inspection activity represents the completion of 3 samples relative to this inspection area (i.e., inspection procedure sections 02.03.a and 02.05.a and b) in partial fulfillment of the annual inspection requirements.

Problem Identification and Resolution (02.03.a)

During this week of inspection, the inspector reviewed the licensees self-assessment activities for any results related to the access control program since the last inspection.

The intent of this review was to determine if identified problems were entered into the corrective action program for resolution.

High Risk Significant, High Dose Rate HRA and VHRA Controls (02.05.a and b)

On February 2 through 5, the inspector met at various times with the Health Physics General Supervisor, the Health Physics Operations Supervisor, and the Health Physics Support Supervisor and discussed the controls and procedures for high-dose-rate high radiation areas (HRAs) and for very high radiation areas (VHRAs). The inspector reviewed the subject procedures (as listed in the List of Documents Reviewed section)to verify that the level of worker protection was adequate.

Related Activities On February 2 and 5, the inspector observed Radiologically-Controlled Area (RCA)entries and exits being made by radiation workers at the primary RCA access control point to verify compliance with requirements for RCA entry and exit, wearing of record dosimetry, and issuance and use of alarming electronic radiation dosimeters. The inspector toured various elevations in the auxiliary building to verify the adequacy of the radiological controls which were being implemented. The inspector reviewed observed work activities for compliance with the special work permit (SWP) requirements. During these observations and tours the inspector reviewed, for regulatory compliance, the posting, labeling, barricading, and level of radiological access control for locked high radiation areas (LHRAs), high radiation areas (HRAs), radiation and contamination areas, and radioactive material areas.

On February 4, the inspector examined the materials processing facility (MPF) and inspected the exteriors of locations used for radioactive material storage outside the protected area, including the independent spent fuel storage installation (ISFSI), the storage building for the old steam generators, and a large fenced storage area (Lake Davies).

On February 5, the inspector observed the morning turnover meetings for the Health Physics (HP) staff and for the HP technicians.

The inspector performed a selective examination of documents (as listed in the List of Documents Reviewed section) to evaluate the adequacy of radiological controls.

The review in this area was against criteria contained in 10 CFR 19.12, 10 CFR 20 (Subparts D, F, G, H, I, and J), Technical Specifications, and procedures.

b. Findings

No findings of significance were identified.

2OS2 ALARA Planning and Controls (71121.02 - 2 samples)

a. Inspection Scope

The inspector reviewed the effectiveness of the licensees program to maintain occupational radiation exposure as low as is reasonably achievable (ALARA). This inspection activity represents the completion of two

(2) samples relative to this inspection area (i.e., inspection procedure sections 02.01.a and 02.03.a) in partial fulfillment of the annual inspection requirements.

Inspection Planning (02.01.a)

Prior to and during this inspection, the inspector reviewed pertinent information regarding plant collective exposure history, current exposure trends, and ongoing or planned activities in order to assess current performance and exposure challenges. The inspector determined the plants three-year rolling average collective exposure through the end of 2002. The inspector also reviewed the sites collective exposure for 2003.

Verification of Dose Estimates and Exposure Tracking Systems (02.03.a)

On February 3, at Warehouse 1, the inspector met with the Health Physics Work Leader (Radiological Engineering). During this meeting, the inspector reviewed the assumptions and basis for the current annual collective exposure estimate including that for the estimate for normal operations and that for the planned Unit 1 refueling outage.

The inspector also reviewed the applicable ALARA procedures used to determine the methodology for estimating work activity-specific exposures and the intended dose outcome.

Related Activities Issues, covered in the above-cited discussions, also included trends in on-line and outage exposures, outage SWPs, exposure tracking systems, the outage estimate breakdown, ALARA reviews, and the activities of the site ALARA committee.

Also, on February 3, at the Office Training Facility (OTF), the inspector met with the Health Physics Support Supervisor and discussed the HP high impact team (HIT) plan for the Unit 1 2004 refuel outage and the HP contingency plans, also for the Unit 1 2004 refuel outage.

On February 4, at Warehouse 1, the inspector observed a meeting of the HP HIT at which the 2004 refueling outage activity schedule for containment (April 9 through April 23, 2004) was reviewed.

The inspector performed a selective examination of documents (as listed in the List of Documents Reviewed section) for regulatory compliance and for adequacy of control of radiation exposure.

The review was against criteria contained in 10 CFR 20.1101 (Radiation protection programs), 10 CFR 20.1701 (Use of process or other engineering controls), and procedures.

b. Findings

No findings of significance were identified.

2OS3 Radiation Monitoring Instrumentation and Protective Equipment (71121.03 - 1 sample)

a. Inspection Scope

The inspector reviewed the program for health physics instrumentation to determine the accuracy and operability of the instrumentation. This inspection activity represents the completion of one

(1) sample relative to this inspection area (i.e., inspection procedure section 02.04.b) in partial fulfillment of the annual inspection requirements.

Problem Identification and Resolution (02.04.b)

During this inspection, the inspector reviewed corrective action program reports related to incidents involving radiation monitoring instrument deficiencies since the last inspection in this area. The inspector interviewed the Health Physics Work Leader (Radiation Instruments) and discussed the reported radiation monitoring deficiencies and their resolution. The inspector also toured the radiation instrumentation calibration facilities in the South Service Building (SSB) and in the Office Training Facility (OTF).

The inspector performed a selective examination of documents (as listed in the List of Documents Reviewed section) for regulatory compliance and adequacy in this area.

The review was against criteria contained in 10 CFR 20.1501, 10 CFR 20 Subpart H, Technical Specifications, and procedures.

b. Findings

No findings of significance were identified.

OTHER ACTIVITIES

40A1 Performance Indicator Verification (71151)

During an EP program inspection conducted in July 2002 (50-317/02-010, 50-318/02-010), the inspector identified an Unresolved Item (URI 50-317/02-010-02, 50-318/02-010-02) regarding the licensees Alert and Notification System (ANS) PI data.

Specifically, due to operational problems because of an aging ANS, the licensee changed their testing methodology to perform three consecutive tests versus one during their weekly silent tests. They chose three tests because at a minimum, one of the three signals would result in a successful activation. However, when reporting the ANS PI data, the licensee considered the three silent tests as one test but was reporting successes on any of the three tests. The inspector determined that by not counting all the tests, the licensee could be unintentionally masking failures which may provide a false impression that the system was operating at a high performance level.

Constellation Generation Group believed the calculation of the data was correct because their testing method mimicked the signal activation of state-of-the-art systems currently being used by other power plants even though their system didnt operate in that manner. Constellation Generation Group submitted a Frequently Asked Question (FAQ) to the Nuclear Energy Institute (NEI) to determine if their interpretation of the guidance set forth in NEI 99-02, Revision 2 is correct and entered the issue in their corrective action system (No. IR3-021-087).

In November 2002, Constellation Generation Group presented their issue before the Reactor Oversight Process (ROP) Working Group Committee. In June 2003, the ROP Working Group Committee decided the issue would be reviewed generically (FAQ No.

35.7) with respect to whether a licensee is able to modify their ANS testing methodology for calculating the site ANS PI data. In February 2004 the FAQ was finalized which included a response specific to the Calvert Cliffs issue. The FAQ response stated it was not necessary for Constellation Generation Group to re-calculate their past PI data from the time of the change; however, the response directed the licensee to update the ANS PI data report by noting they had changed their testing method in the comment section which was submitted with their first quarter 2004 PI data report. Meanwhile, Constellation Nuclear Generation replaced their aging ANS in late 2003 with a newer system and changed their testing methodology back to counting each push as a test to accommodate the operability of the system. URI 50-317/02-010-02, 50-318/02-010-02 is considered closed.

4OA2 Identification and Resolution of Problems

1. Annual Sample Review

a. Inspection Scope

The inspector selected seven issues identified in the Corrective Action Program (CAP)for detailed review (Issue Report Nos. IR4-008-987 and -988, IR4-009-607, -608, -642, and -680, and IR4-023-854). The issues were associated with site dose reduction, inadvertent release of radioactive material from the RCA, position qualifications, completion and documentation of required training, negative trends in written communications identified by self-assessment review, and documentation of radioactive material storage locations. On February 5, the inspector met with the Health Physics Support Supervisor to discuss these Issue Reports. The documented reports for the issues were reviewed to ensure that the full extent of the issues was identified, an appropriate evaluation was performed, and appropriate corrective actions were specified and prioritized.

b. Findings

No findings of significance were identified.

2. Annual Sample Review

a. Inspection Scope

( 1 sample)

The inspector selected Issue Report (IR) IR4-013-246 for detailed review. The IR identified a wall thinning condition downstream of flow orifice 1-FO-3710 in the Unit 1 reheat steam system. The wall thickness remaining was found to be degraded below specification requirements. This piping segment is scheduled for replacement during the refuel outage beginning April 2004, and, is currently restored to full pressure retaining capability by the installation of a mechanical clamp over the degraded area.

The IR was reviewed to ensure a complete and accurate identification of the issue, an appropriate root cause evaluation was performed, extent of condition was considered and corrective actions were specified and verified as completed. The IR and the resolution documents were reviewed against the requirements of Constellation Nuclears corrective action process. The inspector noted that during the review of extent-of-condition activities, the licensee replaced those piping segments downstream of the flow orifice on the remaining three moisture separator reheaters for Units 1 and 2.

The inspector noted that additional issue reports and a self assessment had been recently initiated related to the implementation of the Flow Accelerated Corrosion (FAC)

Program. Consequently, the inspector selected IR4-028-240, IR3-058-986, IR4-013-245, IR4-013-246 and Self Assessment 200200117 for review to assess the effectiveness of the FAC Program in meeting the requirements of NRC Bulletin 87-01 and Generic Letter 89-08 regarding the implementation of a Program to ensure that erosion/corrosion does not lead to degradation of single phase and two phase high-energy carbon steel systems.

The inspector also conducted interviews with personnel responsible for the implementation of the flow accelerated corrosion program to assess the effectiveness of the program to detect degraded pipe wall thickness in high energy applications.

b. Findings

No findings of significance were identified.

3. Effectiveness Of Corrective Actions Associated With Mispositioning Events

a. Inspection Scope

(1 sample)

The inspectors reviewed the licensees corrective action program documents pertaining to component mispositioning events. Including in these were issue reports, causal analysis reports, and previously implemented corrective actions. The inspectors also conducted interviews with various station personnel.

b. Findings

Introduction:

The inspectors identified a self-revealing finding of very low safety significance (Green) which resulted in a non-cited violation (NCV) for the licensees failure to establish adequate corrective actions associated with component mispositioning events as required by 10 CFR Part 50 Appendix B, Criterion XVI, Corrective Actions.

Description:

During the period of time between January 7, 2002 and March 31, 2004, there have been a total of fifty two component mispositioning events which were identified by the licensee and entered into their corrective action program. An NRC problem identification and resolution (PI&R) team inspection, which concluded on November 7, 2003, assessed 45 of these events which occurred between January 7, 2002, and October 28, 2003. This assessment resulted in the identification of a Green finding associated with the licensees failure to adequately establish and implement corrective actions to address the negative trend associated with component mispositionings [Inspection Report IR-2003-009, NCV 05000317; 05000318/2003009-01].

On October 29, 2003, the licensee issued IR4-016-119 to address this negative trend.

As a result, the licensee developed root causal analysis, IR200300402, which identified several underlying causes of the component mispositioning events. This analysis, dated December 23, 2003, provided a number of corrective actions designed to prevent the recurrence of mispositioning events.

Subsequent to these actions, the inspectors reviewed component mispositioning events that occurred between October 29, 2003, and March 31, 2004. These events represented seven of the fifty two events. Four of these events were classified as Category II IRs, which warranted a causal analysis; however, the inspectors determined that only two of these had risk significance. The first event occurred on March 4, 2004, during the performance of STP M-213-1, Calibration of Power Range Instrumentation by Comparison with Incore Nuclear Instrumentation. This STP was being performed on channel D of the Unit 1 Reactor Protection System. During the performance of this test, an instrumentation and controls technician inadvertently placed the channel C operate/test switch to zero. This resulted in a unintended trip condition on channel C, placing the system in a condition where a single failure in either the A or B channels could have resulted in a unit trip. The second event occurred on March 21, 2004, during the performance of OI-2A, Chemical & Volume Control System, Section 6.10, Purge and Establishment of Hydrogen Overpressure, when operators inadvertently closed valve 1-CVC-501, VCT Outlet Isolation. Although this valve was in a closed position for less than a minute, this action resulted in a loss of suction to all three charging pumps, causing the 12 charging pump to trip on low suction head, and causing the 13 charging pump to become gas bound. The 11 charging pump was not running at this time and was immediately available once suction was reestablished to the volume control tank (VCT). In light of these events, the inspectors determined that the licensees corrective actions to address component mispositioning thus far have not been fully effective in preventing component mispositioning events associated with risk significant components.

During the inspectors review of component mispositioning events, the inspectors noted an increase in tagout errors. Specifically, between October 29, 2003, and March 31, 2004, there were four tagout errors. Two of these were associated with safety-related systems, however, the inspectors determined that only one of these errors could have been potentially risk significant. This error involved a clearance order that intended to isolate the 22 service water (SRW) system by closing 2-SW-386, Manual SW Outlet.

The tagout incorrectly directed the closure of 2-SW-253, 21 A/B SRW Heat Exchanger Salt Water Outlet Isolation Valve. Had the tagout been performed as written, saltwater flow to both SRW subsystems would have been isolated, causing both subsystems to become inoperable. As field operators started closing 2-SW-253, 21 Saltwater Flow Trouble alarm was received in the control room. At the same time, field operators recognized changes in flow noises and stopped the tagout evolution, recognizing that the tagout was in error. The inspectors determined that this tagout error did not result in any adverse consequences to the plant, but considered the recent increase in tagout errors to be a contributor to the already identified negative trend of component mispositionings.

Analysis:

The inspectors determined that the ongoing adverse trend specifically associated with the safety-related component mispositioning events mentioned above constituted a significant condition adverse to quality, and that the licensees failure to take appropriate and timely corrective actions to resolve this negative trend constituted a performance deficiency. This finding is greater than minor because it affected the human performance attribute and the availability, reliability, and capability objectives of the mitigating system cornerstone.

The significance of this finding was evaluated in accordance with NRC Manual Chapter 0609, Appendix A, Attachment 1, Significance Determination Process (SDP) for Reactor Inspection Findings for At-Power Situations, and was determined to be of very low safety significance (Green) since none of the events resulted in the actual loss of a system safety function therefore, this issue screened out of the Phase I SDP as a Green finding.

Enforcement:

10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, states in part, that measures shall be established to assure that conditions adverse to quality are promptly identified and corrected; and for significant conditions adverse to quality, the measures shall assure that the cause of the condition is determined and corrective action taken to preclude recurrence. Contrary to the above, two significant conditions adverse to quality involving component mispositioning events associated with safety-related systems occurred between October 29, 2003, and March 31, 2004. These events are a continuance of a previously identified negative trend. The inspectors concluded that in light of the previously identified non-cited violation associated with component mispositioning events, prompt and effective corrective actions have not been adequately established to prevent the recurrence of similar events. Because these mispositioning events were of very low safety significance, and have been entered into the licensees corrective action program as IR4-030-128 and IR4-031-134 respectively, this violation is being treated as a non-cited violation (NCV), consistent with Section VI.A of the NRC Enforcement Policy. NCV 05000317; 05000318/2004-004-02, Failure To Implement Effective Corrective Actions Associated With Component Mispositioning Events.

3. Cross-References to PI&R Findings Documented Elsewhere

Section 1R12 describes a finding for failure to identify a degraded condition regarding a distorted journal cap on the 2A EDG. The licensee had an opportunity to identify the degraded condition in 1995.

4OA3 Event Follow-up (7 samples)

1. (Closed) Licensee Event Report (LER) 50-318/2003-01, Emergency Air Lock

Containment Penetration Closure Requirements Violation On February 24, 2003, plant personnel identified a condition prohibited by technical specifications where a temporary hose penetrating the containment emergency air lock temporary closure device was not sealed, and core alterations had been ongoing.

Specifically, on February 23, core alterations (control element assembly uncoupling)were performed for approximately 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> and the containment emergency air lock temporary closure device was not closed (sealed) for approximately 5 of the 8 applicable hours, as required by technical specifications. The licensee determined the cause to be human error in that work packages were inadequate and there were inadequate communications. The work packages did not provide caution statements or adequately describe containment closure requirements necessary when performing work activities at the emergency air lock temporary closure device penetrations. The site procedure containing these cautions and closure requirements was not included in the work packages. Communications were inadequate in that the requirements for containment closure were not communicated or known to the individuals performing the task.

Corrective actions included changing plant procedures to require installation of chains and signs at the emergency air lock requiring notification of operations prior to entry and to require planners to include containment closure compliance steps in future work packages. This finding is more than minor because the finding is associated with the Barrier Integrity Cornerstone configuration control attribute and affected the cornerstone objective. The finding was considered to have very low safety significance (Green)using Appendix H of the SDP because the event did not occur within 8 days of the start of the outage. The inspector reviewed the procedure changes, and discussed the event and procedure changes with site personnel. This licensee-identified finding involved a violation of technical specifications and enforcement aspects of the violation are discussed in Section 4OA7. This LER is closed.

2. (Closed) Licensee Event Report (LER) 50-318/2003-02, Unintentional Reactor

Protective System (RPS) Actuation During Plant Heatup On April 19, 2003, during startup surveillance testing, while all control element assemblies were fully inserted into the core, Unit 2 received an automatic trip signal due to steam generator low pressure automatic bypass resetting prior to the trip signal reset.

Calvert Cliffs personnel determined that the cause for the event was a combination of setpoint tolerance, system design, and operating conditions. Corrective actions taken included revising related procedures to establish initial conditions such that tests cannot be conducted in the steam generator pressure range where this RPS actuation could occur, and evaluating all other RPS and Engineered Safety Features Actuation System trip inputs for similar unanticipated actuations resulting from configurations currently allowed by procedure. The inspector reviewed the procedure changes, and discussed the event and procedure changes with site personnel. The LER was reviewed by the inspectors and no findings of significance were identified. The licensee documented the event in Issue Report IR4-018-667. This LER is closed.

3. (Closed) Licensee Event Report (LER) 50-318/2003-04-00 & 50-318/2003-04-01,

Technical Specification Exceeded Due to Extended Repair of Diesel Generator On October 10, 2003, the licensee requested a Notice of Enforcement Discretion (NOED) due to the extended repair of the 2A EDG. The licensee determined the root cause of this event to be a human performance deficiency associated with the failure to identify a distorted journal cap in 1995 following an installation error of the journal cap and upper bearing in 1994. Details of this event are provided in Section 1R12 of this report. These LERs are closed.

4. (Closed) Unresolved Item (URI) 50-318/2003-06-02, Review of Previous Maintenance

and Vendor Related Activities Associated with the 2A EDG On October 10, 2003, the NRC granted a Unit 2 NOED related to enforcing compliance with the requirements of Technical Specification(TS) 3.8.1, AC Sources - Operating.

This was based on the licensees inability to perform repair activities on the 2A EDG #10 upper crankcase bearing within the established allowable outage time. The inspectors reviewed the applicable TS requirements, assessed the licensees inspection efforts pertaining to potential common-mode failure mechanisms affecting the other EDGs, and monitored compliance for granting of the NOED as well as the implemented compensatory actions during the extended outage duration.

Details pertaining to the dispositioning of this item are contained in Section 1R12 of this report. This URI is closed.

5. Unit 2 Reactor Trip

a. Inspection Scope

On January 23, 2004, the inspectors responded to the control room to assess plant conditions and operator performance following a Unit 2 reactor trip from 100 percent reactor power. This reactor trip was caused by the inadvertent tripping of the 22 steam generator feed pump which resulted in the lowering of steam generator levels below automatic reactor trip setpoints.

Based on the complicated nature of this trip, which involved multiple equipment malfunctions and operator performance deficiencies, the NRC established a Special Inspection Team (SIT) to perform detailed inspection of this event, and address potential deficiencies associated with the event. This inspection was initiated in accordance with NRC Inspection Procedure 71153 Event Follow-up, and NRC Management Directive 8.3, NRC Incident Investigation Program. The inspection will be conducted in accordance with NRC Inspection Procedure 93812, Special Inspection, and documented in NRC Inspection Report 2004-008.

b. Findings

No findings of significance were identified.

6. Unit 1 Reactor Trip

a. Inspection Scope

On March 20, 2004, the inspectors responded to the control room to assess maintenance activities that were in progress prior to a Unit 1 reactor trip, as well as plant conditions and operator performance following the event. The reactor trip occurred while at 100 percent reactor power. The trip was caused when maintenance activities induced a ground fault which resulted in erratic indications and failures associated with the digital feedwater system.

Based on the time that this event occurred, and in light of the ongoing NRC special inspection associated with the Unit 2 reactor trip mentioned above, the NRC determined to amend the original special inspection charter for the Unit 2 trip event, in order to appropriately assess related factors associated with this trip. Inspection results pertaining to this event will be documented in NRC Inspection Report 2004-008.

b. Findings

No findings of significance were identified.

7. Rapid Downpower Due To Fire Protection System Actuation

a. Inspection Scope

On March 30, 2004, the inspectors responded to the site to evaluate conditions leading up to and following a rapid downpower on Unit 1 from 100 percent to 68 percent reactor power. This downpower was performed as a conservative, anticipatory measure to preclude a potential reactor trip associated with the loss of a steam generator feedwater pump following the actuation of the fire protection system. A sprinkler head contained within an asbestos removal enclosure tent activated after exceeding its temperature setpoint and sprayed down cable trays in the vicinity of digital feedwater system control panels.

The inspectors reviewed station procedures to ensure compliance, performed walkdowns of the affected areas, and conducted discussions with engineering personnel to understand the circumstances that led to the actuation as well as the extent of condition prior to commencing a power increase. Further details pertaining to this event are provided in Section 1R14.

b. Findings

No findings of significance were identified.

4OA5 Other Activities

Spent Fuel Material Control and Accounting at Nuclear Power Plants - Temporary Instruction 2515/154 Temporary Instruction 2515/154, Spent Fuel Material Control and Accounting at Nuclear Power Plants, Phase I and Phase II, were completed during this inspection period.

Appropriate documentation was provided to NRC management as required.

4OA6 Meetings, including Exit

On April 8, 2004, the inspectors presented the inspection results to Kevin Neitmann and other members of his staff. The inspectors confirmed that proprietary information was not provided or examined during the inspection.

4OA7 Licensee-Identified Violations

Technical Specification 3.9.3, Containment Penetrations, requires during core alterations, that the emergency air lock temporary closure device be closed. Contrary to this, on February 23, 2003, the closure device was not closed in that a hose penetrating the closure device was not sealed. This was identified in the corrective action program as IR4-015-307. This finding is of very low safety significance because it did not occur within 8 days of the start of the outage.

ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

J. Ball, Health Physics Work Leader, Radiological Engineering
S. Brown, Health Physics Work Leader, Operations

Bill Carey, Operator

Keith Crissman, Electrical Maintenance

Sonny Dean, Auxiliary Systems Manager

Paul Fatka, System Manager

Dave Frye, Shift Manager

P. Furio, Supervisor, Regulatory Matters
M. Geckle, Operations Manager
J. Gines, Mechanical Engineering Consultant

Chip Grooms, Shift Manager

J. Guidotti, Health Physics Work Leader, Radiation Instruments

Calvin Hancock, Health Physics Supervisor

D. Holm, Manager, Nuclear Maintenance

Mark Hunter, System Manager

S. Hutson, Outage Management
J. Johnson, Health Physics Technician

Al Kelly, Senior Reactor Operator

Keith King, Senior Reactor Operator

T. Kirkham, Radiation Protection Supervisor

Joe Klecha, Operator

Ed Kreahling, System Manager

Hien Le, System Manager

J. Lenhart, Health Physics Work Leader, Operations

Randy Lewis, Operator

S. Loeper, mechanical Engineering Consultant

Dave Lynch, Shift Manager

Dale McElheny, System Manager

Roger McPherson, Operator

Homero Montes De Oca, Electrical Maintenance Supervisor

K. Neitmann, Plant General Manager

Bob Pace, Shift Manager

B. Pickett, Health Physics Technician

Tom Pilkerton, Mechanical Maintenance Supervisor

Mike Polak, Secondary Systems Manager

I. Rice, Health Physics Technician
S. Sanders, General Supervisor, Radiation Safety

Curtis Scayles, Mechanical Maintenance Supervisor

A. Simpson, Regulatory Matters Supervisor
B. Scott, Mechanical Engineering Consultant
G. Vanderheyden, Vice President

Larry Vandersnick, Operator

Larry Williams, Systems Manager

J. York, Health Physics Support Supervisor
M. Yox, Engineering Analyst

LIST OF ITEMS

OPENED, CLOSED AND DISCUSSED

Opened

None

Opened and Closed

050000318/2004-04-01, EA-04-084 NCV Failure To Prevent Recurrence Of A Degraded Bearing Condition (Section 1R12)
05000317;
05000318/2004-04-02 NCV Failure To Implement Effective Corrective Actions Associated With Component Mispositioning Events (Section 4OA2)

50-318/2003-01 LER Emergency Air Lock Containment Penetration Closure Requirements Violation (Section 4OA3)

50-318/2003-02 LER Unintentional Reactor Protective System (RPS)

Actuation During Plant Heatup (Section 4OA3)

50-318/2003-04-00, 01 LER Technical Specification Exceeded Due to Extended Repair of Diesel Generator (Section 4OA3)

Closed

50-317; 318/02-010-02 URI ANS PI Data potentially not being calculated properly. (Section 4OA1)

50-318/2003-06-02 URI Review of Previous Maintenance and Vendor Related Activities Associated with the 2A EDG (Section 4OA3)

LIST OF DOCUMENTS REVIEWED