IR 05000317/2022002

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Integrated Inspection Report 05000317/2022002 and 05000318/2022002
ML22220A038
Person / Time
Site: Calvert Cliffs  Constellation icon.png
Issue date: 08/08/2022
From: Brice Bickett
NRC/RGN-I/DORS
To: Rhoades D
Constellation Energy Generation, Constellation Nuclear
References
IR 2022002
Download: ML22220A038 (17)


Text

August 8, 2022

SUBJECT:

CALVERT CLIFFS NUCLEAR POWER PLANT - INTEGRATED INSPECTION REPORT 05000317/2022002 AND 05000318/2022002

Dear David Rhoades:

On June 30, 2022, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Calvert Cliffs Nuclear Power Plant. On July 14, 2022, the NRC inspectors discussed the results of this inspection with Patrick D. Navin, and other members of your staff. The results of this inspection are documented in the enclosed report.

One finding of very low safety significance (Green) is documented in this report. This finding involved a violation of NRC requirements. We are treating this violation as a non-cited violation (NCV) consistent with Section 2.3.2 of the Enforcement Policy.

If you contest the violation or the significance or severity of the violation documented in this inspection report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN:

Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region I; the Director, Office of Enforcement; and the NRC Resident Inspector at Calvert Cliffs Nuclear Power Plant.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region I; and the NRC Resident Inspector at Calvert Cliffs Nuclear Power Plant. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely, Brice A. Bickett, Branch Chief Projects Branch 3 Division of Operating Reactor Safety

Docket Nos. 05000317 and 05000318 License Nos. DPR-53 and DPR-69

Enclosure:

As stated

Inspection Report

Docket Numbers:

05000317 and 05000318

License Numbers:

DPR-53 and DPR-69

Report Numbers:

05000317/2022002 and 05000318/2022002

Enterprise Identifier: I-2022-002-0031

Licensee:

Constellation Energy Generation, LLC

Facility:

Calvert Cliffs Nuclear Power Plant

Location:

Lusby, MD

Inspection Dates:

April 1, 2022 to June 30, 2022

Inspectors:

R. Clagg, Senior Resident Inspector

L. Dumont, Senior Reactor Inspector

S. Obadina, Resident Inspector

G. Walbert, Project Engineer

D. Werkheiser, Senior Reactor Analyst

Approved By:

Brice A. Bickett, Branch Chief

Projects Branch 3

Division of Operating Reactor Safety

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees

performance by conducting an integrated inspection at Calvert Cliffs Nuclear Power Plant, in

accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs

program for overseeing the safe operation of commercial nuclear power reactors. Refer to

https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

Failure to Perform An Adequate Foreign Material Close-Out Inspection Results in a Unit 2

Manual Reactor Trip

Cornerstone

Significance

Cross-Cutting

Aspect

Report

Section

Initiating Events

Green

NCV 05000318/2022002-01

Open/Closed

[H.12] - Avoid

Complacency

71153

A self-revealed Green finding and associated non-cited violation of Technical Specification 5.4.1, Procedures, was identified when Constellation failed to perform an adequate foreign

material close-out inspection for the 12 spent fuel cooling pump breaker cubicle as required

by site procedures. Specifically, on November 21, 2021, Constellation failed to verify that the

12 spent fuel cooling pump breaker cubicle was free of foreign material as required by MA-

AA-716-008, Foreign Material Exclusion Program, Revision 16, which resulted in a Unit 2

manual reactor trip.

Additional Tracking Items

Type

Issue Number

Title

Report Section

Status

LER 05000318/2022-001-00

LER 2022-001-00 for Calvert

Cliffs Nuclear Power Plant,

Unit 2, Automatic Reactor Trip Due to High Reactor

Coolant System Pressure

71153

Closed

LER 05000318/2021-004-00

LER 2021-004-00, Calvert

Cliffs Nuclear Power Plant,

Unit 2, Manual Reactor Trip

Due to Lowering Steam

Generator Levels

71153

Closed

PLANT STATUS

Unit 1 operated at or near rated thermal power for the entire inspection period.

Unit 2 operated at or near rated thermal power for the entire inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in

effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with

their attached revision histories are located on the public website at http://www.nrc.gov/reading-

rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared

complete when the IP requirements most appropriate to the inspection activity were met

consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection

Program - Operations Phase. The inspectors performed activities described in IMC 2515,

Appendix D, Plant Status, observed risk significant activities, and completed on-site portions of

IPs. The inspectors reviewed selected procedures and records, observed activities, and

interviewed personnel to assess licensee performance and compliance with Commission rules

and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

Seasonal Extreme Weather (IP Section 03.01) (1 Sample)

(1)

The inspectors evaluated readiness for seasonal extreme weather conditions prior to

the onset of seasonal hot temperatures for the Units 1 and 2 emergency diesel

generators and intake structures on May 12, 2022

71111.04 - Equipment Alignment

Partial Walkdown (IP Section 03.01) (4 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following

systems/trains:

(1)

Unit 1, 12 and 13 saltwater pumps and associated equipment with 11 saltwater pump

out of service for maintenance, April 29, 2022

(2)

Unit 1, 1B emergency diesel generator, 0C diesel generator, and associated

equipment with 1A emergency diesel generator out of service for maintenance,

May 5, 2022

(3)

Unit 1, 11 saltwater air compressor and associated equipment with 12 saltwater air

compressor out of service for maintenance, June 7, 2022

(4)

Unit 2, 21 emergency core cooling system and associated components with 22

emergency core cooling system air cooler out of service for maintenance,

June 14, 2022

Complete Walkdown Sample (IP Section 03.02) (1 Sample)

(1)

The inspectors evaluated system configurations during a complete walkdown of the

Unit 1 high-pressure safety injection system on June 28, 2022.

71111.05 - Fire Protection

Fire Area Walkdown and Inspection (IP Section 03.01) (5 Samples)

The inspectors evaluated the implementation of the fire protection program by conducting a

walkdown and performing a review to verify program compliance, equipment functionality,

material condition, and operational readiness of the following fire areas:

(1)

Units 1 and 2, cable chases and control room complex, fire areas 20-24,

May 12, 2022

(2)

Units 1 and 2, horizontal chases and 69' elevation electrical rooms, fire areas 35-38,

May 12, 2022

(3)

0C (station blackout) diesel generator building, fire area EDG0C, May 17, 2022

(4)

Unit 2, east and west electrical penetration rooms, fire areas 26-27, May 25, 2022

(5)

Unit 1, east and west electrical penetration rooms, fire areas 32-33, June 1, 2022

Fire Brigade Drill Performance (IP Section 03.02) (1 Sample)

(1)

The inspectors evaluated the on-site fire brigade training and performance during an

unannounced fire drill at the machine shop on June 8, 2022.

71111.07A - Heat Exchanger/Sink Performance

Annual Review (IP Section 03.01) (1 Sample)

The inspectors evaluated readiness and performance of:

(1)

Unit 1, 12 component cooling heat exchanger maintenance and testing,

June 22, 2022

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)

(1)

The inspectors observed and evaluated licensed operator performance in the control

room during Unit 1, 'B' train safety injection valve testing on June 8, 2022.

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

(1)

The inspectors observed licensee operator training involving a steam leak inside

containment, a loss of auxiliary feedwater common suction, and a loss of offsite

power in the simulator on June 15, 2022.

71111.12 - Maintenance Effectiveness

Maintenance Effectiveness (IP Section 03.01) (1 Sample)

The inspectors evaluated the effectiveness of maintenance to ensure the following

structures, systems, and components (SSCs) remain capable of performing their intended

function:

(1)

Unit 1, AR 4445774, control element assembly dropped during power ascension,

reviewed on May 2, 2022

Quality Control (IP Section 03.02) (1 Sample)

The inspectors evaluated the effectiveness of maintenance and quality control activities to

ensure the following SSC remains capable of performing its intended function:

(1)

Unit 1, WO C93780548, 11A service water heat exchanger relief valve replacement,

May 24, 2022

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management (IP Section 03.01) (7 Samples)

The inspectors evaluated the accuracy and completeness of risk assessments for the

following planned and emergent work activities to ensure configuration changes and

appropriate work controls were addressed:

(1)

Unit 1, elevated risk condition due to 11 saltwater pump out of service for

replacement, May 10, 2022

(2)

Unit 1, elevated risk condition due to 1A emergency diesel generator out of service

for maintenance, May 12, 2022

(3)

Unit 2, elevated risk condition due to 22 component cooling heat exchanger out of

service for maintenance, May 24, 2022

(4)

Unit 1, elevated risk condition due to 11A service water heat exchanger out of service

for maintenance, May 27, 2022

(5)

Unit 2, risk informed completion time implementation due to channel 'A' reactor

protection system issues, May 31, 2022

(6)

Unit 1, elevated risk condition due to 12 containment air cooler out of service for

maintenance, June 13, 2022

(7)

Unit 1, elevated risk condition due to 1B emergency diesel generator out of service

for maintenance, June 29, 2022

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 03.01) (4 Samples)

The inspectors evaluated the licensee's justifications and actions associated with the

following operability determinations and functionality assessments:

(1)

Unit 1, AR 4493073, U-4000-11, 14 kilovolt transformer, upper left fan blade sheared

preventing rotation, April 19, 2022

(2)

Unit 2, AR 4493548, gap between wall and frame for emergency hatch #2 (high

energy line break barrier), May 24, 2022

(3)

Unit 1, AR 4501988, 12 containment air cooler local control hand switch failed to

operate in the high position, May 27, 2022

(4)

Unit 1, AR 4501259, dissolved gas analyzer for U-4000-13, 4 kilovolt transformer, in

alarm status, May 31, 2022

71111.18 - Plant Modifications

Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02) (1

Sample)

The inspectors evaluated the following temporary or permanent modifications:

(1)

Unit 2, ECP-17-000204, Ovation turbine control megawatt transducer circuit

modification, June 29, 2022

Severe Accident Management Guidelines Update (IP Section 03.03) (1 Sample)

(1)

The inspectors verified the site's severe accident management guidelines were

updated in accordance with the pressurized water reactor generic severe accident

technical guidelines and validated in accordance with Nuclear Energy Institute 14-01,

Emergency Response Procedures and Guidelines for Beyond Design Basis Events

and Severe Accidents, Revision 1, on June 7, 2022.

71111.19 - Post-Maintenance Testing

Post-Maintenance Test (IP Section 03.01) (8 Samples)

The inspectors evaluated the following post-maintenance testing activities to verify system

operability and/or functionality:

(1)

Unit 1, WO C93756168, 1CV5159A, 12A service water heat exchanger saltwater

strainer flushing valve replacement and testing, April 15, 2022

(2)

Unit 1, WO C93702979, 11 saltwater pump replacement, April 28, 2022

(3)

Unit 1, WO C93751562, perform emergency diesel generator-13 on 1A1 and 1A2

emergency diesel generator engines, May 6, 2022

(4)

Unit 1, WO C93783627, perform speed control knob torque check of 11 auxiliary

feedwater turbine governor, May 10, 2022

(5)

Unit 1, WO C93752186, replace paper drive assembly for 1RE5280, containment

atmosphere particulate radiation monitoring system, May 12, 2022

(6)

Unit 1, WO C93649176, 13 saltwater pump motor replacement, May 24, 2022

(7)

Unit 2, WO C93670498, 22 emergency core cooling system air cooler maintenance

and testing, June 15, 2022

(8)

Unit 2, WO C93783966, 21 instrument air dryer maintenance and testing,

June 30, 2022

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance testing activities to verify system operability

and/or functionality:

Surveillance Tests (other) (IP Section 03.01) (2 Samples)

(1)

Unit 2, STP-O-008A(SA)-2, "Test of 2A DG and 4kV Bus 21 Undervoltage," Revision

35, April 28, 2022

(2)

Unit 2, STP-O-5A22-2, "22 Auxiliary Feedwater Pump Quarterly Surveillance Test,"

Revision 9, May 5, 2022

Inservice Testing (IP Section 03.01) (1 Sample)

(1)

Unit 1, WO C93782745, STP-O-65C3-1, "14 CAC SRW Inlet, 1CV1592, Quarterly

Operability Test," Revision 2, May 12, 2022

71114.06 - Drill Evaluation

Select Emergency Preparedness Drills and/or Training for Observation (IP Section 03.01) (1

Sample)

(1)

The inspectors observed and evaluated the conduct of an Emergency Preparedness

drill involving the failure of a containment sump motor operator valve with an

earthquake which causes flooding from the 12 saltwater header rupture and service

water pump room, and the loss of the 14 safety-related bus with the loss of cooling

accident on hot leg resulting in a General Emergency declaration on May 10, 2022.

OTHER ACTIVITIES - BASELINE

71151 - Performance Indicator Verification

The inspectors verified licensee performance indicators submittals listed below:

MS05: Safety System Functional Failures (IP Section 02.04) (2 Samples)

(1)

Unit 1, April 1, 2021 through March 31, 2022

(2)

Unit 2, April 1, 2021 through March 31, 2022

71152S - Semiannual Trend Problem Identification and Resolution

Semiannual Trend Review (Section 03.02) (1 Sample)

(1)

The inspectors reviewed the licensees corrective action program for potential

adverse trends that might be indicative of a more significant safety issue.

71153 - Follow Up of Events and Notices of Enforcement Discretion

Event Report (IP Section 03.02) (2 Samples)

The inspectors evaluated the following licensee event reports (LERs):

(1)

LER 05000318/2021-004-00, Manual Reactor Trip Due to Lowering Steam Generator

Levels, (Agencywide Documents Access and Management System (ADAMS)

Accession No. ML22018A025). The inspection conclusions associated with this LER

are documented in this report under Inspection Results.

(2)

LER 05000318/2022-001-00, Automatic Reactor Trip Due to High Reactor Coolant

System Pressure (ADAMS Accession No. ML22063A703). The inspectors determined

that the cause of the condition described in the LER was not reasonably within the

licensees ability to be foreseen and corrected and, therefore, was not reasonably

preventable. No performance deficiency nor violation of NRC requirements was

identified.

INSPECTION RESULTS

Observation: Semiannual Trend Review

71152S

The inspectors identified an adverse trend associated with degraded reactor coolant system

Tcold resistance temperature detectors for the Unit 1 and 2 reactor protection systems.

Constellation entered the following issues into their corrective action program in order to be

appropriately addressed.

  • On December 8, 2021, as documented in AR 4465414, following surveillance testing

Constellation identified that the Tcold temperature element for channel 'A' of the

reactor protection system on Unit 2 was found to have failed low. Further investigation

identified that the temperature element was degraded. The temperature element was

replaced during a forced outage.

  • On April 26, 2022, as documented in AR 4495809, control room operators received an

unexpected alarm and determined that the Tcold indication for reactor protection

system channel 'A' was erratic. Constellation replaced the temperature transmitter and

power supply, and restored channel 'A' of reactor protection system on Unit 2 to

service after satisfactory testing.

  • On May 23, 2022, as documented in AR 4501587, Constellation identified that the

Unit 2 reactor protection system channel 'A' Tcold indication was rising unexpectedly.

Constellation performed troubleshooting and determined that the temperature element

needed to be replaced or repaired. The reactor protection system is designed such

that two temperature elements provide indication, and the highest temperature is

selected. Constellation removed the degraded temperature element from service and

has actions to repair or replace the temperature element during the next refueling

outage. The second temperature element is in service and providing appropriate

indication.

  • On June 28, 2022, as documented in AR 4508003, Constellation identified that the

Tcold indication for channel 'C' of the reactor protection system on Unit 1 was

indicating higher than normal. Constellation performed troubleshooting and

determined that the power supply was degraded. Constellation replaced the power

supply and returned channel 'C' of reactor protection system to service after

satisfactory testing. In AR 4465778, Constellation documented a potential cause for

the degraded Tcold indications as loose or degraded connections at the resistance

temperature detectors quick disconnect wiring harnesses and has sent these items

offsite for evaluation.

The inspectors review noted Constellation has an action to document the final determination

of the cause for the degraded resistance temperature detectors due in August of 2022. In

addition, the inspectors noted degraded power supplies have caused some of the Tcold

indication issues. In AR 4508003, Constellation has an action to review the reactor protection

system power supply failure history and revise the preventive maintenance strategy as

appropriate. The inspectors determined these deficiencies demonstrate an adverse trend with

regards to degraded Tcold resistance temperature detectors and Constellation generated

ARs 4465414, 4465778, 44995809, 4501587, and 4508003 to address the deficiencies. The

NRC inspectors did not identify any findings or violations of more than minor significance

during this review.

Failure to Perform An Adequate Foreign Material Close-Out Inspection Results in a Unit 2

Manual Reactor Trip

Cornerstone

Significance

Cross-Cutting

Aspect

Report

Section

Initiating Events

Green

NCV 05000318/2022002-01

Open/Closed

[H.12] - Avoid

Complacency

71153

A self-revealed Green finding and associated non-cited violation of Technical Specification 5.4.1, Procedures, was identified when Constellation failed to perform an adequate foreign

material close-out inspection for the 12 spent fuel cooling pump breaker cubicle as required

by site procedures. Specifically, on November 21, 2021, Constellation failed to verify that the

12 spent fuel cooling pump breaker cubicle was free of foreign material as required by MA-

AA-716-008, Foreign Material Exclusion Program, Revision 16, which resulted in a Unit 2

manual reactor trip.

Description: On November 21, 2021, Constellation was in the process of performing post-

maintenance testing on the 12 spent fuel cooling pump and breaker. When starting the pump,

an arc flash event occurred in the breaker. As a result, the upstream breaker (24A 480 volt

bus feeder breaker) tripped open. This caused a loss of bus 2Y10, which is a non-vital 120

volt AC instrument bus. The loss of bus 2Y10 led to the repositioning of Unit 2 condensate

pump mini-flow valve, condensate booster pump mini-flow valve, and moisture separator

reheater drain tank high level dump valve, which created a secondary transient. This resulted

in the 21 steam generator feedwater pump (SGFP) tripping on low-suction pressure. The 23

SGFP started due to the trip of the 21 SGFP. However, the loss of bus 2Y10 also caused a

loss of the control element drive system and created an inability for the station to manually

move control rods, which is needed when using the 23 SGFP following a loss of either 21 or

22 SGFPs. At 10:46 am, without the ability to manually insert control element assemblies to

lower reactor power, Unit 2 was manually tripped from 100 percent power due to lowering

steam generator levels. Constellation manually initiated auxiliary feedwater to maintain level

in the steam generators. From this event, Constellation submitted LER 05000318/2021-004-

00.

The inspectors reviewed Constellation's root cause investigation, AR 4462339, and noted

that foreign material in the 12 spent fuel cooling pump breaker cubicle caused the arc flash

event. The foreign material was identified as insulating breaker cubicle stab covers that are

used to protect plant personnel from energized parts. The root cause investigation stated that

the installation of breaker cubicle stab covers without a tracking mechanism, which were not

removed from the breaker cubicle following maintenance, was the root cause. The inspectors

reviewed the procedures associated with breaker cubicle maintenance and electrical safety.

Specifically, the inspectors reviewed FTE-53A, Westinghouse 480 Volt Load Center Cubicle

Maintenance, Revision 0002, which provides a warning that the stationary main stabs remain

energized with 480 volt AC. In addition, the inspectors reviewed SA-AA-129, Electrical

Safety, Revision 11, which provides direction for installing insulating covers for energized

parts. Specifically, it states, in part, that the licensee should install protective shields when a

breaker is removed from a compartment and energized bus bars are exposed. The inspector

noted that while the procedures provided direction for installing insulating covers, the

procedures did not provide a tracking mechanism or removal instructions for the insulating

breaker cubicle stab covers.

The inspectors reviewed WO C93680525 for the breaker cubicle maintenance and noted that

it included documentation for the foreign material close-out inspection and also identified the

work as a foreign material exclusion zone 2. The inspectors reviewed the MA-AA-716-008-F-

01, Work Package Device and Close-out Form, Revision 1, which requires that a final close-

out inspection be performed, where the individual verifies that the system/component is free

of foreign material prior to final system closure. This form was completed in the work package

indicating that the foreign material close-out inspection had been performed. The inspectors

also reviewed MA-AA-716-008, Revision 16, which provided a definition for foreign material

exclusion zone 2, which is a zone that is established in situations where a final visual internal

inspection is possible prior to system closure. The inspectors also reviewed step 14.1.6, of

MA-AA-716-008, Revision 16, which states, in part, that the licensee shall verify that the

system internals, components, and parts being installed are free of foreign materials prior to

reassembly. The inspectors determined that a foreign material close-out inspection should

have identified the insulating breaker cubicle stab covers. The inspectors concluded that the

licensee performed an inadequate foreign material close-out inspection, which resulted in a

Unit 2 manual reactor trip.

Corrective Actions: Constellation revised procedure FTE-53A to prohibit the use of stab

covers during breaker cubicle inspections. Constellation removed all stab covers from the

shop and verified that supply chain does not have any future orders to purchase additional

stab covers.

Corrective Action References: AR 4462339

Performance Assessment:

Performance Deficiency: Constellation's failure to perform an adequate foreign material

close-out inspection was a performance deficiency. WO C93680525 classified the work as

foreign material exclusion zone 2, which requires the use of licensee procedure, MA-AA-716-

008, Foreign Material Exclusion Program, Revision 16. Specifically, step 14.1.6, states, in

part, that the lead worker shall verify that the system internals, components and parts, being

installed are free of foreign materials prior to reassembly. Contrary to this, Constellation failed

to verify that the 12 spent fuel cooling pump breaker cubicle was free of foreign material,

specifically, the insulating breaker cubicle stab covers in the breaker cubicle. As a result, an

arc flash event occurred in the 12 spent fuel cooling pump breaker which subsequently

required a Unit 2 manual reactor trip.

Screening: The inspectors determined the performance deficiency was more than minor

because it was associated with the Human Performance attribute of the Initiating Events

cornerstone and adversely affected the cornerstone objective to limit the likelihood of events

that upset plant stability and challenge critical safety functions during shutdown as well as

power operations. Specifically, the failure to perform an adequate foreign material close-out

inspection of the 12 spent fuel cooling pump breaker cubicle resulted in an arc flash event

inside the breaker and subsequently required a Unit 2 manual reactor trip.

Significance: The inspectors assessed the significance of the finding using IMC 0609

Appendix A, The Significance Determination Process (SDP) for Findings At-Power. The

inspectors screened this finding for safety significance and determined that a detailed risk

evaluation was required. Specifically, the finding caused a reactor trip and loss of mitigating

equipment relied upon to transition the plant from a reactor trip to a stable shutdown

condition.

The performance deficiency caused the loss of the 480 volt load center 24A, motor control

centers 125/204R, and 120 volt instrument bus 2BUS2Y10. This resulted in a low-suction

pressure trip of the 21 SGFP due to the loss-of-power failed-open position of minimum flow

bypass valves and loss of manual reactor rod control (both due to loss of 2BUS2Y10),

necessitating a manual reactor trip by the operators. The subsequent loss of the 22 SGFP on

high-discharge pressure after the reactor trip was not considered related to the performance

deficiency. This initiating event was evaluated as a transient/reactor trip. However, the senior

reactor analysts also evaluated the event as a loss of main feedwater to ensure a bounding

sensitivity review was performed.

The regional senior reactor analysts used the Systems Analysis Programs for Hands-On

Evaluation, Revision 8.2.6, and the Standardized Plant Analysis Risk Model for Calvert Cliffs

Unit 2, Model Version 8.64, to conduct an initiating event analysis. This included

consideration of the effect on systems, structures, and components that were impacted by the

performance deficiency.

In accordance with IMC 0308 and Risk Assessment of Operational Events Handbook

guidance, the Significance Determination Process evaluates the risk increase/significance of

the performance deficiency that causes an initiating event by using the incremental

conditional core damage probability estimate:

Incremental conditional core damage probability = Conditional core damage probability -

Baseline core damage probability

The initiating event was set to 1.0, including any inclusive systems, structures, and

component failures, and the conditional core damage probability was calculated by the

Systems Analysis Programs for Hands-On Evaluation. For this finding, the initiating event

transient/reactor trip was set to 1.0. For the loss of main feedwater sensitivity case, event loss

of main feedwater was set to 1.0. The following additional standardized plant analysis risk

model modifications were made:

21 SGFP (MFW-TDP-FR-PUMP21) set to 0.2, as a surrogate for recovery, (21 SGFP

was recovered shortly after instrument bus 2Y10 was cross-tied to 2Y09, which

provided power to the min-flow valves restoring suction pressure)

AC Bus 24A (ACP-BAC-LP-24A) set to TRUE, (bus was restored 7.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> after

event). This also fails motor control center 125 / 204R and associated loads

Instrument Bus 2Y10 (ACP-BAC-LP-2Y10) failure probability was increased by an

order of magnitude, as a surrogate for recovery, (2Y10 was cross-tied to 2Y09 in 7

minutes per the direction of abnormal operating procedure (AOP-07I-2))

After discussions with Idaho National Labs, motor control center 204R fault tree was

modified to account for short term recovery probability to cross-tie to motor control

center 214R via procedure. A Standardized Plant Analysis Risk-H human error

probability was calculated to be 0.14 for high-stress, moderate complexity, and

minimum time to complete. (conditional core damage probability results were

insensitive to variations to this basic event)

(Sensitivity) Alignments of key equipment were set to run TRUE or standby FALSE.

This was performed to realistically assess the important risk contributors due to the

cross-train capability and flexibilities modeled in the Calvert Cliff Unit 2 standardized

plant analysis risk model

The following influential assumptions were used:

Transient/reactor trip best represented the initiating event

21 SGFP loss was directly related to the performance deficiency; 22 SGFP was lost

after the reactor trip due to an unexpected feedwater system response after receiving

its expected reactor trip override and speed runback and is not considered related to

this performance deficiency

Standby electric feedwater pump (23 SGFP), which started once the 21 SGFP was

lost, subsequently tripped as designed, coincident with the reactor trip and hence is

considered to have little to no mitigating impact to the initiating event

Recovery of feedwater and buses 2Y10/125/204R were feasible and justified

Bus 24A was not readily recoverable based on troubleshooting and repairs. The

licensee provided a damage assessment and justification for possible early recovery,

but the senior reactor analysts did not consider this in the risk assessment

Nominal test and maintenance values; A sensitively case was performed with key

equipment alignments set as existed during the event (loss of main feedwater, service

water, and switchgear ventilation)

Senior reactor analysts preliminary risk assessments determined the finding to be risk

significant and identified dominant event trees as medium-break loss of coolant accidents and

anticipated transients without scram. The dominant sequences involved loss of reactor

coolant pump seals, failure to trip reactor coolant pumps, and high-pressure injection failure.

This was similar for both transient/reactor trip and loss of main feedwater (sensitivity) initiating

event assessments. Further review of dominant sequence cut sets indicated this was mainly

the result of motor control center 204R failure, loss of component coolant water, and

emergency switchgear cooling that results in failure of emergency switchgear loads. This

makes the conditional core damage probability results highly sensitive to alternate switchgear

ventilation (as proceduralized in OI-22H) and the failure probability of the portable generators

powering those fans. A review of calculation CA04570, that documents heat-up of the Unit 1

and 2 switchgear rooms on loss of ventilation, indicates that up to 13 hours1.50463e-4 days <br />0.00361 hours <br />2.149471e-5 weeks <br />4.9465e-6 months <br /> is available to

establish alternate ventilation before exceeding operational temperature limits for the affected

emergency switchgear. Therefore, the senior reactor analysts concluded that this supported a

low failure probability of the emergency switchgear loads from a loss of ventilation. Based on

additional discussions with Constellation and considering the last bus was recovered within

7.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> after the event, additional standardized slant analysis risk model adjustments were

made:

Alternate emergency switchgear ventilation power (ACP-MGN-FC-PORTGEN) was

reduced by two orders of magnitude to account for the large number of units tested

and available

Operator action to establish alternate emergency ventilation (HVC-XHE-XM-

RMCOOL) was reduced by an order of magnitude to account for the large available

time to establish the alternate line-up

  • Various basic event probability updates based on senior reactor analyst's discussions

with licensee probabilistic risk assessment staff to account for plant recoveries over

the 7.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> of the event

The calculated conditional core damage probability for a transient with the above adjustments

was 8.2E-7. The baseline core damage probability was calculated to be 2.1E-7.

The incremental conditional core damage probability was 8.2E-7 - 2.1E-7, which resulted in a

risk increase 6.1E-7. The dominant sequence is a transient, with loss of reactor coolant pump

seals (from the loss of component cooling water), failure to trip reactor coolant pumps, and

failure of high-pressure injection.

A sensitivity case treating the event as a loss of main feedwater was conducted and resulted

in similar conditional core damage probability results and dominant sequences. The loss of

main feedwater case was sensitive to the 21 SGFP recovery and availability of low-pressure

feedwater. Both transient/reactor trip and loss of main feedwater risk analyses were

insensitive to crediting diverse and flexible mitigation strategies (i.e., FLEX).

The performance deficiency did cause a transient (reactor trip), however an external event

that could cause a transient cannot cause the performance deficiency to be revealed. The

senior reactor analysts validated through discussions with NRC inspectors, review of the

licensees root cause analysis, etc. that the performance deficiency will only have a risk

impact when connecting the affected breaker to the bus. Therefore, the risk can be assessed

looking only at internal events and risk contribution due to fire, flood, tornado, or seismic

events need not be considered.

A large early release frequency assessment was made using the Systems Analysis Programs

for Hands-On Evaluation and IMC 0609, Appendix H, dated March 23, 2020. The Systems

Analysis Programs for Hands-On Evaluation calculated increase in large early release

frequency was <1E-7 based on zero-factor multipliers for dominant sequences. Also, since

Calvert Cliffs Unit 2 is a combustion engineering designed pressurized water reactor a

separate consequential steam generator tube rupture screening was performed in

accordance with IMC 0609, Appendix H, Section 5, aided by NUREG-2195, Consequential

SGTR Analysis for Westinghouse and Combustion Engineering Plants, Appendix L, dated

July 2017. Since all dominant sequence large early release frequency factors were zero, this

assessment screened out having very low safety significance

Constellation also performed an analysis of the performance deficiency using the Calvert

Cliffs Unit 2 full-power internal events application-specific model based on the model of

record and provided it to the analysts for information. The senior reactor analysts reviewed

the analysis, key inputs, and assumptions and determined that their analysis was consistent

with the NRC method. The licensees calculated incremental conditional core damage

probability was 7.83E-7 with similar dominant sequences identified by the senior reactor

analysts evaluation.

In summary, the increase in risk associated with the performance deficiency using the

incremental conditional core damage probability estimate is 6.1E-7 and represents a finding

of very low safety significance (Green). Incremental conditional core damage probability or

delta core damage frequency are the risk metrics for the Significance Determination Process

to evaluate the significance of inspection findings, and their numerical values are consistent

with the risk informed scale and basis detailed in IMC 0308.

Cross-Cutting Aspect: H.12 - Avoid Complacency: Individuals recognize and plan for the

possibility of mistakes, latent issues, and inherent risk, even while expecting successful

outcomes. Individuals implement appropriate error reduction tools. Specifically, Constellation

failed to recognize the task of installing insulating breaker cubicle stab covers introduced

foreign material into the breaker cubicle and should have recognized and planned for the

possibility of mistakes.

Enforcement:

Violation: The Renewed Facility Operating License for Calvert Cliffs Power Plant, Unit 2,

Technical Specification 5.4.1 requires, in part, that written procedures shall be established,

implemented, and maintained as covered in Regulatory Guide 1.33, Revision 2, Appendix A,

February 1978, where Section 9a specifies that maintenance that can affect the performance

of safety-related equipment should be properly pre-planned and performed in accordance

with written procedures, documented instructions or drawings. MA-AA-716-008, Foreign

Material Exclusion Program, Revision 16, step 14.1.6 states, in part, that the lead worker

shall verify that the system internals, components, and parts, being installed are free of

foreign materials prior to reassembly.

Contrary to the above, on November 21, 2021, Constellation failed to satisfactorily implement

MA-AA-716-008 for the 12 spent fuel cooling pump and breaker maintenance. Specifically,

Constellation did not perform an adequate foreign material close-out inspection and left the

insulating breaker cubicle stab covers installed in the breaker cubicle. This resulted in an arc

flash event inside the breaker and subsequently required a Unit 2 manual reactor trip.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with

Section 2.3.2 of the Enforcement Policy.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On July 14, 2022, the inspectors presented the integrated inspection results to Patrick D.

Navin, and other members of the licensee staff.