IR 05000317/2023003

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Integrated Inspection Report 05000317/2023003 and 05000318/2023003
ML23305A105
Person / Time
Site: Calvert Cliffs  Constellation icon.png
Issue date: 11/01/2023
From: Brice Bickett
Division of Operating Reactors
To: Rhoades D
Constellation Energy Generation, Constellation Nuclear
References
IR 2023003
Download: ML23305A105 (1)


Text

November 1, 2023

SUBJECT:

CALVERT CLIFFS NUCLEAR POWER PLANT, UNITS 1 AND 2 -

INTEGRATED INSPECTION REPORT 05000317/2023003 AND 05000318/2023003

Dear David Rhoades:

On September 30, 2023, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Calvert Cliffs Nuclear Power Plant, Units 1 and 2. On October 11, 2023, the NRC inspectors discussed the results of this inspection with Patrick Navin, Site Vice President, and other members of your staff. The results of this inspection are documented in the enclosed report.

One Severity Level IV violation without an associated finding is documented in this report. We are treating this violation as a non-cited violation (NCV) consistent with Section 2.3.2 of the Enforcement Policy.

No NRC-identified or self-revealing findings were identified during this inspection.

If you contest the violation or the significance or severity of the violation documented in this inspection report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN:

Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region I; the Director, Office of Enforcement; and the NRC Resident Inspector at Calvert Cliffs Nuclear Power Plant, Units 1 and 2. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations (10 CFR) 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely, Brice A. Bickett, Chief Projects Branch 3 Division of Operating Reactor Safety

Docket Nos. 05000317 and 05000318 License Nos. DPR-53 and DPR-69

Enclosure:

As stated

Inspection Report

Docket Numbers:

05000317 and 05000318

License Numbers:

DPR-53 and DPR-69

Report Numbers:

05000317/2023003 and 05000318/2023003

Enterprise Identifier: I-2023-003-0027

Licensee:

Constellation Energy Generation, LLC

Facility:

Calvert Cliffs Nuclear Power Plant, Units 1 and 2

Location:

Lusby, MD

Inspection Dates:

July 01, 2023 to September 30, 2023

Inspectors:

G. Dipaolo, Senior Resident Inspector

A. Tran, Resident Inspector

C. Borman, Health Physicist

R. Clagg, Senior Project Engineer

L. Dumont, Senior Reactor Inspector

N. Eckhoff, Health Physicist

E. Eve, Senior Project Engineer

J. Lilliendahl, Senior Emergency Response Coord

K. Mangan, Senior Reactor Inspector

S. Mercurio, Emergency Preparedness Inspector

Approved By:

Brice A. Bickett, Chief

Projects Branch 3

Division of Operating Reactor Safety

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Calvert Cliffs Nuclear Power Plant, Units and 2, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors.

Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

Unit 2 Pressurizer Safety Valve Inoperable for Greater than Technical Specification Allowed Time Cornerstone Severity Cross-Cutting Aspect Report Section Not Applicable Severity Level IV NCV 05000318/2023003-01 Open/Closed Not Applicable 71153 A self-revealed Severity Level IV non-cited violation of Technical Specification 3.4.10,

"Pressurizer Safety Valves," was identified when the lift setpoint of the Unit 2 pressurizer safety valve, 2RV200, was found below the technical specification allowable value.

Additional Tracking Items

Type Issue Number Title Report Section Status LER 05000318/2022-003-00 LER 2022-003-00 for Calvert Cliffs Nuclear Power Plant,

Unit No. 2, Pressurizer Safety Valve As-Found Settings (Low) Outside Technical Specification Limits Due to Setpoint Drift 71153 Closed

PLANT STATUS

Unit 1 began the inspection period at rated thermal power. On September 30, 2023, the unit was down powered to 13 percent power to facilitate containment entry to address increased unidentified reactor coolant system leakage. The unit ended the inspection period at approximately 70 percent power, with operators continuing to increase power to full rated thermal power.

Unit 2 operated at or near rated thermal power for the entire inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed activities described in IMC 2515, Appendix D, Plant Status, observed risk significant activities, and completed on-site portions of IPs. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

Impending Severe Weather Sample (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated the adequacy of the overall preparations to protect risk significant systems from impending severe weather due to a tornado watch being issued for Calvert County, Maryland on August 7, 2023.

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (3 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1) Unit 2, 2B emergency diesel generator following scheduled work being delayed due to a leak on a fuel return line, August 17, 2023
(2) Unit 2, 22 component cooling water heat exchanger train when the 21 train was inoperable due to planned maintenance, August 30, 2023
(3) Unit 2, 22 and 23 component cooling water pump trains when the 21 component cooling water pump was unavailable due to planned maintenance, September 28, 2023

71111.05 - Fire Protection

Fire Area Walkdown and Inspection Sample (IP Section 03.01) (5 Samples)

The inspectors evaluated the implementation of the fire protection program by conducting a walkdown and performing a review to verify program compliance, equipment functionality, material condition, and operational readiness of the following fire areas:

(1) Units 1 and 2, auxiliary feedwater pump rooms, fire areas 42 and 43, July 3, 2023
(2) Units 1 and 2, 1B, 2A, and 2B emergency diesel generator rooms, fire areas 28, 30, and 31, July 11, 2023
(3) Unit 1, 11 and 12 emergency core cooling system pump rooms, fire areas 3 and 4, August 8, 2023
(4) Units 1 and 2, intake structure, fire area IS, August 8, 2023
(5) Units 1 and 2, outside yard area and buildings, fire area Yard, August 24, 2023

Fire Brigade Drill Performance Sample (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated the on-site fire brigade training and performance during an unannounced fire drill in the Unit 2 turbine building on September 27, 2023.

71111.07A - Heat Exchanger/Sink Performance

Annual Review (IP Section 03.01) (1 Sample)

The inspectors evaluated readiness and performance of:

(1) Unit 2, 21 component cooling water heat exchanger thermal performance test, September 22, 2023

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (2 Samples)

(1) The inspectors observed and evaluated operator performance in the main control room following Unit 2 entry into Abnormal Operating Procedure 3G-2, "Malfunction of Feedwater System," due to 22 heater drain tank high level and normal level control valves failing closed resulting from a loss of instrument air on August 1, 2023.
(2) The inspectors observed and evaluated licensed operator performance in the main control room during Unit 1 power maneuvers to/from 13 percent power to facilitate containment entry on September 30, 2023.

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

(1) The inspectors observed and evaluated a licensed operator simulator examination involving secondary plant and electrical system failures causing reactor reactivity changes, secondary failures requiring a manual reactor scram, and grid instability that caused a station blackout resulting in the declaration of a General Emergency on August 1, 2023.

71111.12 - Maintenance Effectiveness

Maintenance Effectiveness (IP Section 03.01) (2 Samples)

The inspectors evaluated the effectiveness of maintenance to ensure the following structures, systems, and components (SSCs) remain capable of performing their intended function:

(1) Unit 2, AR 4693777, 2A emergency diesel generator received an automatic start blocked alarm while filling the jacket cooling water expansion tank, August 10, 2023
(2) Unit 2, AR 4688144, excessive leak on 22 service water system causing header inoperability, September 9, 2023

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated the accuracy and completeness of risk assessments for the following planned and emergent work activities to ensure configuration changes and appropriate work controls were addressed:

(1) Unit 2, elevated risk condition due to 21 auxiliary feedwater pump being inoperable because of isolation of 21 steam generator steam admission valve, 2-MS-4070, due to leakage, July 27, 2023
(2) Unit 2, elevated risk condition due to 21 auxiliary feedwater pump being out of service for turbine overspeed maintenance and testing, August 28, 2023
(3) Unit 2, elevated risk condition due to loss of SY01, 120-volt vital AC bus, and implementation of emergent risk-informed risk completion time, September 22, 2023
(4) Units 1 and 2, elevated risk condition due to 500 kilovolt red bus outage maintenance window, September 22, 2023

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 03.01) (5 Samples)

The inspectors evaluated the licensee's justifications and actions associated with the following operability determinations and functionality assessments:

(1) Unit 1, AR 4688495, 1A emergency diesel generator, April 24, 2023, failure mode causal table open legs, July 20, 2023
(2) Unit 2, AR 4683895, 21 component cooling heat exchanger outlet saltwater branch pipe through-wall leak and use of Title 10 of the Code of Federal Regulations (CFR)50.69(d), "Alternative Treatment Requirements," August 11, 2023
(3) Units 1 and 2, AR 4693044, 1A emergency diesel generator failure root cause extent of condition to the 0C emergency diesel generator functionality assessment, August 31, 2023
(4) Unit 2, AR 4701476, long term trends indicate possible 22A reactor coolant pump seal degradation, September 18, 2023
(5) Units 1 and 2, AR 4704844, diverse and flexible coping strategies (FLEX) auxiliary feedwater pump annual functional testing not performed in accordance with program requirements and preventative maintenance template, September 26, 2023

71111.18 - Plant Modifications

Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02) (1 Sample)

The inspectors evaluated the following temporary or permanent modifications:

(1) ECP-20-000608, "Formalize the Existing Technical Bases for TA-220 into One Technical Evaluation and 50.59 Screen," Revision 0, September 18, 2023

71111.24 - Testing and Maintenance of Equipment Important to Risk

The inspectors evaluated the following testing and maintenance activities to verify system operability and/or functionality:

Post-Maintenance Testing (PMT) (IP Section 03.01) (6 Samples)

(1) Unit 1, WO C93847891, 12 saltwater pump replacement, July 7, 2023
(2) Unit 1, WO C93913020, 1A emergency diesel generator post-maintenance test following fuel injector replacement, July 16, 2023
(3) Unit 2, WO C93936673, 21 auxiliary feedwater pump steam supply valve from 21 steam generator, 2-MS-4070, post-maintenance test following repairs due to leakage, July 31, 2023
(4) Unit 2, WO C93798835, 21 auxiliary feedwater pump post-maintenance testing following turbine overspeed maintenance, August 30, 2023
(5) Unit 1, WO C93941333, 1A emergency diesel generator post-maintenance test monitoring per abnormal condition monitoring plan, September 25, 2023
(6) Unit 2, WO C93866188, 21 component cooling water pump supply breaker, 2BK52-2106, inspection post-maintenance test, September 28, 2023

Surveillance Testing (IP Section 03.01) (4 Samples)

(1) Unit 1, STP-O-5A11-1, "11 Auxiliary Feedwater Pump Quarterly Surveillance Test,"

Revision 11, July 10, 2023

(2) Unit 2, STP-O-B2YR-2, "Biennial Test of 2B DG," Revision 4, July 18, 2023
(3) Unit 2, STP-O-731-2, "High Pressure Safety Injection Pump and Check Valve Quarterly Test," Revision 13, on the 22 high pressure safety injection pump, August 9, 2023
(4) Unit 1, STP-O-8A-1, "Test of 1A DG and 11 4 kilovolt Bus Undervoltage," Revision 37, August 18, 2023

Diverse and Flexible Coping Strategies (FLEX) Testing (IP Section 03.02) (1 Sample)

(1) Units 1 and 2, WO C93856275, annual vendor maintenance of FLEX equipment located in robust building, September 22, 2023

71114.02 - Alert and Notification System Testing

Inspection Review (IP Section 02.01-02.04) (1 Sample)

(1) As a result of the 2020 COVID-19 Public Health Emergency, the licensee requested and received an exemption to reschedule their biennial emergency preparedness exercise from 2020 to 2021. The inspectors performed the emergency preparedness program inspection scheduled for 2021 in its place, then performed emergency preparedness exercise inspections in 2021 and 2022.

The inspectors evaluated the licensee's maintenance and testing of the station alert and notification system on September 11 through September 14, 2023, for the period of August 2020 through August 2023.

71114.03 - Emergency Response Organization Staffing and Augmentation System

Inspection Review (IP Section 02.01-02.02) (1 Sample)

(1) The inspectors evaluated the readiness of the licensee's Emergency Preparedness Organization on September 11 through September 14, 2023.

71114.04 - Emergency Action Level and Emergency Plan Changes

Inspection Review (IP Section 02.01-02.03) (1 Sample)

(1) The inspectors evaluated the following submitted Emergency Action Level and Emergency Plan changes:
  • 23-07, EP-AA-112-200-F-14, Technical Service Center Radiation Protection Manager Checklist, Revision U/EP-AA-112-400-F-16; Emergency Operations Facility Radiation Protection Manager Checklist, Revision N
  • 22-68, EP-AA-120-F-06, Evacuation Time Estimate Review Checklist, Revision C

This evaluation does not constitute NRC approval.

71114.05 - Maintenance of Emergency Preparedness

Inspection Review (IP Section 02.01 - 02.11) (1 Sample)

(1) The inspectors evaluated the maintenance of the emergency preparedness program on September 11 through September 14, 2023, for the period of August 2020 through August 2023.

71114.06 - Drill Evaluation

Drill/Training Evolution Observation (IP Section 03.02) (1 Sample)

(1) The conduct of an emergency response drill in the control room simulator and Technical Support Center involving failures that resulted in the declaration of a General Emergency on September 6,

RADIATION SAFETY

71124.08 - Radioactive Solid Waste Processing & Radioactive Material Handling, Storage, &

Transportation

Radioactive Material Storage (IP Section 03.01)

The inspectors evaluated the licensees performance in controlling, labeling and securing the following radioactive materials:

(1) Materials processing facility dry active waste storage areas
(2) Lake Davies radioactive waste storage area

Radioactive Waste System Walkdown (IP Section 03.02) (2 Samples)

The inspectors walked down the following accessible portions of the solid radioactive waste systems and evaluated system configuration and functionality:

(1) Waste gas decay tanks and pumps
(2) Advanced liquid processing system radioactive waste processing system in auxiliary building

Waste Characterization and Classification (IP Section 03.03) (2 Samples)

The inspectors evaluated the following characterization and classification of radioactive waste:

(1) Characterization of type B package #W23-004 (2)2022/2023 Part 61 dry active waste stream characterization and analysis

Shipment Preparation (IP Section 03.04) (1 Sample)

(1) The inspectors observed the preparation of radioactive shipment U231328 on September 14, 2023

Shipping Records (IP Section 03.05) (4 Samples)

The inspectors evaluated the following non-excepted radioactive material shipments through a record review:

(1) UN2916 Radioactive material, Type B package, Shipment number #W23-004
(2) UN2916 Radioactive material, Type B package, Shipment number #W22-006
(3) UN3321 Radioactive material, low specific activity (LSA-II), Shipment number #W22-005
(4) UN2912 Radioactive material, low specific activity (LSA-I), Shipment number #W23-

OTHER ACTIVITIES - BASELINE

===71151 - Performance Indicator Verification

The inspectors verified licensee performance indicators submittals listed below:

IE01: Unplanned Scrams per 7000 Critical Hours Sample (IP Section 02.01)===

(1) Unit 1, July 1, 2022 through June 30, 2023
(2) Unit 2, July 1, 2022 through June 30, 2023

IE04: Unplanned Scrams with Complications (USwC) Sample (IP Section 02.03) (2 Samples)

(1) Unit 1, July 1, 2022 through June 30, 2023
(2) Unit 2, July 1, 2022 through June 30, 2023

MS07: High Pressure Injection Systems (IP Section 02.06) (2 Samples)

(1) Unit 1, October 1, 2022 through June 30, 2023
(2) Unit 2, October 1, 2022 through June 30, 2023

OR01: Occupational Exposure Control Effectiveness Sample (IP Section 02.15) (1 Sample)

(1) September 1, 2022 through August 31, 2023

PR01: Radiological Effluent Technical Specifications/Offsite Dose Calculation Manual Radiological Effluent Occurrences (RETS/ODCM) Radiological Effluent Occurrences Sample (IP Section 02.16) (1 Sample)

(1) September 1, 2022 through August 31, 2023

EP01: Drill/Exercise Performance (DEP) Sample (IP Section 02.12) (1 Sample)

(1) July 1, 2022 through June 30, 2023

EP02: Emergency Response Organization (ERO) Drill Participation (IP Section 02.13) (1 Sample)

(1) July 1, 2022 through June 30, 2023

EP03: Alert And Notification System (ANS) Reliability Sample (IP Section 02.14) (1 Sample)

(1) July 1, 2022 through June 30, 2023

71152A - Annual Follow-up Problem Identification and Resolution Annual Follow-up of Selected Issues (Section 03.03)

The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:

(1) AR 4524139, pressurizer safety relief valve RV 200 (S/N BV02950) test results below technical specification requirements

71153 - Follow-Up of Events and Notices of Enforcement Discretion Event Report (IP Section 03.02)

The inspectors evaluated the following licensee event reports (LERs):

(1) LER 05000318/2022-003-00, "Pressurizer Safety Valve As-Found Settings (Low)

Outside Technical Specification Limits Due to Setpoint Drift," (Agencywide Documents Access and Management System (ADAMS) Accession No.

ML22325A332). The inspectors determined that it was not reasonable to foresee or correct the cause discussed in the LER; therefore, no performance deficiency was identified. The inspection conclusions associated with this LER are documented in this report under the Inspection Results section, Severity Level IV NCV.

Personnel Performance (IP Section 03.03) (1 Sample)

(1) The inspectors evaluated Unit 2, AR 4703527, loss of 120-volt vital AC instrument bus 2Y01 requiring entry into Abnormal Operating Procedure, 7J, "Loss of 120 Volt Vital AC or 125 Volt Vital DC Power," Revision 19, on September 19,

INSPECTION RESULTS

Observation: Unit 2 Safety Relief Valve Leakage 71152A The inspectors reviewed the licensee's apparent cause evaluation performed to determine the reasons pressurizer safety valve, 2RV200, leaked during 2021-2022 operations and was subsequently found to have an as-found lift setpoint below the range required by the applicable technical specification surveillance. Operators shutdown Unit 2 in September 2022 to replace the valve due to increased valve seat leakage.

The inspectors noted that the licensee staff had concluded the most likely cause of the valve leak was, in part, related to the removal of procedural steps in Operating Procedure (OP)-01-2, "Start Up from Cold Shutdown." The steps required operators to hold pressure for 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> at a reduced pressure/temperature and then slowly increase pressure to normal operating pressure during startups from cold conditions. The inspectors reviewed licensee corrective action program document, PDR 94068, and noted that it added the steps to OP-01-2 in 1996 as a corrective action to address pressurizer safety valve leakage. The inspectors noted that the hold and slow ascent to normal operating pressure were performed to allow the pressurizer and pressurizer safety valves to reach thermal equilibrium prior to increasing pressurizer temperatures as required to raise reactor coolant system pressure to normal operating pressure. The inspectors review of PDR94068 identified the steps were added to reduce thermal stresses on the pressurizer safety valve in order to minimize seat distortion and minimize the possibility of leakage past the pressurizer safety valve seat.

The inspectors noted other causes were identified by licensee staff along with implementing corrective actions. These included actions taken to address valve deficiencies identified during the inspection of the valve at the test facility, actions to upgrade all pressurizer safety stems to Inconel (previously stainless steel), and changes to the valve test procedures requiring a valve rebuild if the valves were cycled more than 15 times during as-left testing.

These steps were taken to minimize the potential for stem distortions both during test and during operational transients that may cause or contribute to valve leakage. The inspectors determined that the actions taken by the licensee addressed the deficiencies identified.

The inspectors reviewed the circumstances involved with removing procedural steps from OP-01-2 to thermally soak the pressurizer safety valves on plant startup. The inspectors noted that while Unit 2 was being returned to operation from a refueling outage in March 2021, operations management requested licensee engineering staff to evaluate the removal of these steps. Licensee staff determined this was acceptable because the pressure hold was a legacy requirement from PDR94068 and there was not a required basis to continue to perform the hold.

The inspectors concluded the licensees change to OP-01-2 to remove thermally soaking the 2RV200 pressurizer safety valve missed an opportunity to address this operating experience in their review. The inspectors noted licensee's procedure to evaluate changes to procedures, AD-AA-101, "Processing of Procedures, T&RMs, and Forms," stated that for procedure revisions affecting plant equipment, the reviewer should consider operating experience from internal and external sources. The procedure stated in part, "whenever possible, do not limit the operating experience review to the station corrective action program data base, include other databases in the operating experience review." The inspectors reviewed Electric Power Research Institute Nuclear Maintenance Applications Center, "Safety and Relief Valve Testing and Maintenance Guide," 2015, and noted Section 6.14 suggested pressurized water reactor pressurization rates for plant heat up, provided guidance on pressure/temperature increases during plant startup, and specifically stated that rapid pressure/temperature increase rates can cause pressurizer safety valve leakage. The maintenance guide recommended several 2-hour hold times and pressure/temperature rate increase limits to minimize the possibility of valve leakage.

The inspectors considered that the Electric Power Research Institute document described operating experience applicable to pressurizer safety valves and plant startup best practices.

The inspectors concluded the licensees change to OP-01-2 to remove thermally soaking the 2RV200 pressurizer safety valve missed an opportunity to address this operating experience in their review. Additionally, the inspectors observed that while the licensee's apparent cause evaluation identified these steps should be restored and took corrective action to do so, the evaluation did not address other aspects of operations and engineering staff performance that resulted in this decision. The licensee entered this issue into their corrective action program as AR 4692235. The inspectors determined no performance deficiency existed because the applicable procedure steps in AD-AA-101 involved guidance and there were other potential causes contributing to the 2RV200 pressurizer safety valve leak-by condition.

Unit 2 Pressurizer Safety Valve Inoperable for Greater than Technical Specification Allowed Time Cornerstone Severity Cross-Cutting Aspect Report Section Not Applicable Severity Level IV NCV 05000318/2023003-01 Open/Closed

Not Applicable 71153 A self-revealed Severity Level IV non-cited violation of Technical Specification 3.4.10, "Pressurizer Safety Valves," was identified when the lift setpoint of the Unit 2 pressurizer safety valve, 2RV200, was found below the technical specification allowable value.

Description:

The inspectors reviewed LER 2022-003-00 to determine if performance deficiencies and/or violations of NRC regulatory requirements had occurred. In July 2021, while Unit 2 was operating, pressurizer safety valve, 2RV200 (serial number BN02950),began leaking by the seat. Constellation implemented action to monitor the 2RV200 leakage.

In September 2022, when leakage rates exceeded 20 gallons/hour, operators shutdown the unit. Constellation replaced the valve with a previously tested safety relief valve and operators restarted the plant. On September 21, 2022, Constellation had the valve tested at an offsite facility and found the relief setpoint to be lower than the technical specification allowable value (tested value of 2470 pounds per square inch atmospheric (PSIA) versus a technical specification lower limit of 2475 PSIA). The inspectors noted that the relief valve's analyzed lower technical specification setpoint was to minimize the possibility of an inadvertent lift of the relief valve and the analyzed high lift setpoint, 2575 PSIA, was to ensure reactor vessel pressure safety limits were not exceeded. As a result, Constellation operated Unit 2 in violation of Technical Specification 3.4.10 because the valve had been inoperable for a period greater than the allowed completion time specified in Technical Specification 3.4.10.

The inspectors noted that Constellation's apparent cause evaluation found that the lower setpoint lift was most likely caused by a combination of setpoint drift and valve leakage. The inspector's review noted that setpoint drift is a known cause for valves to lift at lower or higher setpoints, and valve leakage will lower lift setpoints but the magnitude of the effect involves uncertainty. The inspectors determined that there was no performance deficiency because it was not reasonable for Constellation to foresee and correct the pressurizer safety valve, 2RV200, being outside the technical specification limits while the valve was installed while the unit was in Mode 1 and 2.

Corrective Actions: Constellation staff replaced the valve with a previously tested safety relief valve and operators restarted the plant.

Corrective Action References: AR 4524139

Performance Assessment:

The NRC determined this violation was not reasonably foreseeable and preventable by the licensee and therefore is not a performance deficiency.

Enforcement:

Severity: The Reactor Oversight Process's significance determination process does not specifically consider a violation of requirements with no performance deficiency in its assessment of licensee performance. Therefore, it is necessary to address this violation which does not include an identified performance deficiency using traditional enforcement rather than assign a color (e.g., Green).

Section 6.1.d of the NRC Enforcement Policy provides examples of Severity Level IV violations. Section 6.1.d.1 states, in part, that failure to comply with the allowances for limiting condition for operation and surveillance requirement applicabilities in Technical Specification, Section 3.0, is an example of a Severity Level IV violation.

Violation: Technical Specification 3.4.10, Pressurizer Safety Valves, required two pressurizer safety valves to be operable during Modes 1 and 2, and in Mode 3 when all reactor coolant system cold leg temperatures are greater than 301°F. With one pressurizer safety valve inoperable, Technical Specification 3.4.10, Condition A, required the inoperable valve to be restored within 15 minutes. If this was not completed or if two pressurizer safety valves were inoperable, then Technical Specification 3.4.10, Condition B, applied which required the unit to be in Mode 3 within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> AND the unit to be cooled down to below 301°F within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />.

Contrary to the above, for a period of time, between March 2021 to September 2022, the Unit 2 pressurizer safety valve, 2RV200, lift setpoint was below the technical specification allowable value causing it to be inoperable and the required actions of Technical Specification 3.4.10 were not performed within the required completion times.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On October 11, 2023, the inspectors presented the integrated inspection results to Patrick Navin, Site Vice President, and other members of the licensee staff.
  • On September 14, 2023, the inspectors presented the radioactive solid waste processing and radioactive material handling, storage, and transportation inspection results to Pete Moodie, Plant Manager and other members of the licensee staff.
  • On September 14, 2023, the inspectors presented the emergency preparedness program inspection results to Pete Moodie, Plant Manager, and other members of the licensee staff.

THIRD PARTY REVIEWS

Inspectors reviewed Institute of Nuclear Power Operations reports that were issued during the inspection period.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.01

Procedures

OP-CA-108-111-

1001

Severe Weather Preparation

006

OP-CA-108-3.0

Immediate Actions

009 00

WC-AA-101

On-Line Work Control Process

71111.04

Procedures

OI-16-2

Component Cooling System

4000

71111.05

Corrective Action

Documents

Resulting from

Inspection

AR 4695243

Fire Extinguisher Not Meeting Acceptance Criteria in Intake

Structure

Procedures

FFSM-13

NFPA 805 Fire Area: 3, Unit 1, No. 12 ECCS Pump Room

FFSM-14

NFPA 805 Fire Area: 4, Unit 1, No. 11 ECCS Pump Room

FFSM-145

NFPA 805 Fire Area: COMP-TB/NSB/ACA

OP-AA-201-003

Fire Drill Performance

71111.07A

Calculations

CA 06924

Evaluation of ET 01-004(5)R: Single Tube Thermal

Performance Testing of 11(21) and 12(22) Component

Cooling Water Heat Exchanger (2002-2006)

M-93-041

Component Cooling Water Heat Exchangers

Procedures

ER-AA-340-1001

GL 89-13 Program Implementation Instructional Guide

71111.11Q Procedures

2C03-ALM

Condensate and Feedwater Control Alarm Manual

07100

AOP-3G-2

Malfunction of Main Feedwater System

71111.12

Corrective Action

Documents

AR 4688144

Excessive Leak on 22 SRW System Causing Header

Inoperability

07/01/2023

Drawings

63086, Sheet

27

Schematic Diagram Diesel Generator 20 Engine Control

Engineering

Changes

ECP-16-000462

Update Fairbanks Morse Diesel Generators Trip Circuit

Design 1A, 2A, and 2B Emergency Diesel Generators

000

ECP-18-000339

Fairbanks Morse LS Circuit Seal-In Contact Modification

000

Engineering

Evaluations

4688144

SRW System Excessive Leak Past Operability Evaluation

07/01/2023

Miscellaneous

Fairbanks Morse Calvert Cliffs NPP-PO Report, Analysis

and Recommendations-Speed Switch Problems

01/05/2016

71111.13

Corrective Action

AR 4699761

Protected Boundary Not Encompassing Valve 2SW5208

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Documents

Resulting from

Inspection

Miscellaneous

Final RICT record

2Y01

Final RICT Record 2Y01

09/21/2023

Procedures

CA-PRA-005.058

Reactor Protective System Notebook

ER-CA-600-201

Calvert Cliff RICT System Guidelines

OP-AA-108-118

Risk-Informed Completion Time

71111.15

Corrective Action

Documents

AR 4701476

Long Term Trends Indicate Possible 22A RCP Seal

Degredation

09/10/2023

Corrective Action

Documents

Resulting from

Inspection

AR 4687682

Incomplete 10 CFR 50.69 Alternate Treatment Application

AR 4687954

OP-AA-108-115, Attachment 6, Need Review and Revision

Based on 10 CFR 50.69 Alternate Treatment Requirements

Engineering

Evaluations

ECP-23-000237

Evaluation of Through-Wall Leak on Saltwater Pipe 2LJ-1-

2011

Miscellaneous

AT-23-0096

Saltwater RISC-3 2" Piping ASME XI Alternative Treatment

Operability

Evaluations23-005

1A EDG: April 24th Failure FMCT Open Legs

71111.18

Corrective Action

Documents

AR 4700327

Transition to Max Tcold Required

09/02/2023

Engineering

Changes

ECP-20-000608

Formalize the Existing Tech Bases for TA-220 Into One

Technical Evaluation and 50.59 Screen

Procedures

TA-220

Temporary Removal of Degraded RPS Temperature Input

0300

71111.24

Corrective Action

Documents

Resulting from

Inspection

AR 4690050

Errors in 12 Saltwater Pump In-Service Test Evaluation

Following Pump Replacement

07/12/2023

AR 4691428

Fuel Leak on 2B Emergency Diesel Generator 8N Fuel

Injector Return Fitting

07/19/2023

AR 4691553

Several Fuel Injector Return Line Fittings on 2B Emergency

Diesel Generator are Cross-Threaded

07/20/2023

Procedures

CC-AA-118

Diverse and Flexible Coping Strategies (FLEX), Spent Fuel

Pool Instrumentation (SFPI), and Harden Containment Vent

System (HCVS) Program Document

I-069-2

Main Steam to Auxiliary Feedpump Air Regulator

00100

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Adjustments

OP-CA-108-106-

0001

Calvert Cliffs Operability and Maintenance Testing

001

STP-O-008A-1

Test of 1A Diesel Generator and 11 4 KV Bus Undervoltage

03700

STP-O-5A21-2

Auxiliary Feedwater Pump Quarterly Surveillance Test

STP-O-73APP-1

Saltwater Pump Replacement Preservice Test

VALVE-02

Auxiliary Feedwater Steam Supply Valve Inspections

00900

Work Orders

C93819722

STP-O-8B2YR-2 Biennial Test Of 2B DG

07/19/2023

C93842991

STP-O-008A-1, 1A DG & 11 4KV Bus LOCI Sequencer

Monthly Test

08/18/2023

C93847891

Replace 12 Saltwater Pump and Inspect Couplings

06/27/2023

C93848019

Auxiliary Feedwater Pump Quarterly Surveillance Test

07/10/2023

C93856275

Sponsor Annual Vendor Maintenance of FLEX Equipment

Located in Robust Building

09/15/2023

71114.02

Miscellaneous

Calvert Cliffs Nuclear Power Plant Alert and Notification

System Design Report

71114.04

Procedures

EP-AA-120-1001

CFR 50.54(q) Change Evaluation

71114.05

Corrective Action

Documents

AR 4702547

AR 4702575

Miscellaneous

KLD TR - 1278, Calvert Cliffs Nuclear Power Plant

Development of Evacuation Time Estimates

09/07/2022

EP-AA-1000

Exelon Nuclear Standardized Radiological Emergency Plan

EP-AA-1011

Exelon Nuclear Radiological Emergency Plan Annex for

Calvert Cliffs Station

71152A

Calculations

ECP-12-000124

CCNPP PSV Setpoint Tolerance

Corrective Action

Documents

3002005362

Nuclear Maintenance Application Center: Safety and Relief

Valve Testing and Maintenance Guide

2015

PDR 94068

AR 4524139

Corrective Action

Documents

Resulting from

Inspection

AR 4692235

Miscellaneous

Traveler # 22-349 BV 02950

09/21/2022

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Traveler # 18-68 BM 07952

09/26/2019

50.59 Screen OP-

01-2

Plant Startup from Cold Shutdown

03300

LER 318-2022-

003

Pressurizer Safety Valve As-found Settings (low) Outside

Technical Specification Limits Due to Setpoint Drift

ML15279A191

Calvert Cliffs Nuclear Power Plant, Units 1 and 2 License

Amendment No. 315

2/30/2015

PO 00543176

BV 02950

03/05/2015

PO 00683031

BN02950 19-89

2/27/2019

PO 00816876

BN04375 Traveler 21-59

06/06/2022

PO 599874

BN04375 Traveler 17-44

01/31/2019

Procedures

AD-AA-101

Processing of Procedures, T&RMs, and Forms

31