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| issue date = 11/12/2009
| issue date = 11/12/2009
| title = IR 05000244-09-008; 06/15/2009 - 06/19/2009 and 08/24/2009 - 08/27/2009; R. E. Ginna Nuclear Plant; Special Inspection Team Report
| title = IR 05000244-09-008; 06/15/2009 - 06/19/2009 and 08/24/2009 - 08/27/2009; R. E. Ginna Nuclear Plant; Special Inspection Team Report
| author name = Lew D C
| author name = Lew D
| author affiliation = NRC/RGN-I/DRP
| author affiliation = NRC/RGN-I/DRP
| addressee name = Carlin J T
| addressee name = Carlin J
| addressee affiliation = R. E. Ginna Nuclear Power Plant, LLC
| addressee affiliation = R. E. Ginna Nuclear Power Plant, LLC
| docket = 05000244
| docket = 05000244
| license number = DPR-018
| license number = DPR-018
| contact person = Clifford J W
| contact person = Clifford J
| case reference number = EA-09-249
| case reference number = EA-09-249
| document report number = IR-09-008
| document report number = IR-09-008
Line 15: Line 15:
| page count = 29
| page count = 29
}}
}}
See also: [[followed by::IR 05000244/2009008]]
See also: [[see also::IR 05000244/2009008]]


=Text=
=Text=
{{#Wiki_filter:UNITED STATES NUCLEAR REGULATORY  
{{#Wiki_filter:UNITED STATES
COMMISSION  
                                  NUCLEAR REGULATORY COMMISSION
REGION I 475 ALLENDALE  
                                                      REGION I
ROAD KING OF PRUSSIA, PA 19406-1415  
                                                475 ALLENDALE ROAD
November 12, 2009 EA-09-249  
                                            KING OF PRUSSIA, PA 19406-1415
Mr. John T. Carlin Vice President, RE. Ginna Nuclear Power Plant RE. Ginna Nuclear Power Plant, LLC 1503 Lake Road Ontario, New York 14519  
                                          November 12, 2009
RE. GINNA NUCLEAR POWER PLANT -NRC SPECIAL INSPECTION  
EA-09-249
TEAM REPORT 05000244/2009008;  
Mr. John T. Carlin
PRELIMINARY  
Vice President, RE. Ginna Nuclear Power Plant
WHITE FINDING Dear Mr. Carlin: On June 16-20, 2009, and August 24-27,2009, the U.S. Nuclear Regulatory  
RE. Ginna Nuclear Power Plant, LLC
Commission (NRC) conducted  
1503 Lake Road
the onsite portions of a special inspection  
Ontario, New York 14519
at RE. Ginna Nuclear Power Plant. office inspection  
SUBJECT:        RE. GINNA NUCLEAR POWER PLANT - NRC SPECIAL INSPECTION TEAM
reviews were conducted  
                REPORT 05000244/2009008; PRELIMINARY WHITE FINDING
in the intervening  
Dear Mr. Carlin:
weeks. The enclosed report documents  
On June 16-20, 2009, and August 24-27,2009, the U.S. Nuclear Regulatory Commission (NRC)
the inspection  
conducted the onsite portions of a special inspection at RE. Ginna Nuclear Power Plant. In
team's findings and observations  
office inspection reviews were conducted in the intervening weeks. The enclosed report
which were discussed  
documents the inspection team's findings and observations which were discussed with you and
with you and others members of your staff on August 27, 2009, during a preliminary  
others members of your staff on August 27, 2009, during a preliminary exit briefing, and on
exit briefing, and on October 7, 2009, during the final exit meeting. The special inspection  
October 7, 2009, during the final exit meeting.
was conducted  
The special inspection was conducted in response to a turbine driven auxiliary feedwater
in response to a turbine driven auxiliary  
(TDAFW) pump overspeed trip on May 26, 2009. The team included a subsequent overspeed
feedwater (TDAFW) pump overspeed  
trip on July 2,2009 into its inspection scope. The NRC's initial evaluation of this condition
trip on May 26, 2009. The team included a subsequent  
satisfied the criteria in NRC Inspection Manual Chapter 0309, "Reactive Inspection Decision
overspeed  
Basis for Reactors," for conducting a special inspection. The basis for initiating this special
trip on July 2,2009 into its inspection  
inspection is further discussed in the inspection team's charter that is included in this report as
scope. The NRC's initial evaluation  
Attachment B.
of this condition  
The inspection examined activities conducted under your license as they relate to safety and
satisfied  
compliance with the Commission's rules and regulations and with the conditions of your license.
the criteria in NRC Inspection  
The inspectors reviewed selected procedures and records, observed activities, and interviewed
Manual Chapter 0309, "Reactive  
personnel.
Inspection  
This letter transmits one self-revealing finding that, using the reactor safety Significance
Decision Basis for Reactors," for conducting  
Determination Process (SOP), has preliminarily been determined to be White, a finding with low
a special inspection.  
to moderate safety significance. The finding is associated with the failure to preclude
The basis for initiating  
recurrence of a significant condition adverse to quality associated with the corrosion of the
this special inspection  
governor control valve of the turbine driven auxiliary feedwater (TDAFW) pump, that led to a
is further discussed  
failure of the TDAFW pump during surveillance testing on July 2, 2009 and was the likely cause
in the inspection  
of the overspeed trip on May 26, 2009. Following the July test failure, Ginna replaced the
team's charter that is included in this report as Attachment  
B. The inspection  
examined activities  
conducted  
under your license as they relate to safety and compliance  
with the Commission's  
rules and regulations  
and with the conditions  
of your license. The inspectors  
reviewed selected procedures  
and records, observed activities, and interviewed  
personnel.  
This letter transmits  
one self-revealing  
finding that, using the reactor safety Significance  
Determination  
Process (SOP), has preliminarily  
been determined  
to be White, a finding with low to moderate safety significance.  
The finding is associated  
with the failure to preclude recurrence  
of a significant  
condition  
adverse to quality associated  
with the corrosion  
of the governor control valve of the turbine driven auxiliary  
feedwater (TDAFW) pump, that led to a failure of the TDAFW pump during surveillance  
testing on July 2, 2009 and was the likely cause of the overspeed  
trip on May 26, 2009. Following  
the July test failure, Ginna replaced the
J. Carlin 2 governor control valve stem and conducted
weekly monitoring
of the governor control valve during surveillance
testing to identify any potential
for stem binding. In addition, corrective
actions included a follow-up
inspection
of the governor control valve during the fall 2009 refueling
outage. There is no immediate
safety concern present due to this finding
because the system is now operable and the long term corrective
actions are being implemented
in Ginna's corrective
action program. The final resolution
of this finding
will be conveyed in a separate correspondence.
As discussed
in the attached Inspection
report. the tinding is also an apparent violation
of NRC requirements.
specifically, 10 CFR Appendix B, Criterion
XVI. "Corrective
Actions." and is therefore
being considered
for escalated
enforcement
action in accordance
with the Enforcement
Policy, which can be found on the NRC's Web site at http://www.nrc.gov/readingrm/doc-collections/enforcementl.
Following
a discussion
of the preliminary
safety Significance
of this finding during the initial exit briefing on August 27,2009. a phone call was held between Glenn Dentel, Branch Chief, Division of Reactor Projects.
and yourself on October 1. 2009. During this call, you indicated
that R.E. Ginna Nuclear Power Plant does not contest the characterization
of the rIsk significance
of this finding, and therefore
you have declined to further discuss this issue at a Regulatory
Conference
or provide a written response.
Please note that by declining
to request a Regulatory
Conference
or submit a written response, you relinquished
your right to appeal the final SOP determination.
in that by not doing either, you would not meet the appeal requirements
stated in the Prerequisite
and Limitation
sections of Attachment
2 of IMC 0609. You will be advised by a separate correspondence
of the results of our deliberations
on this matter. In addition.
the report documents
two findings of very low safety significance (Green). The findings involved violations
of NRC requirements.
However, because of the very low safety significance
and because they are entered into your corrective
action program (CAP). the NRC is treating these findings as non-cited
violations (NeVs) consistent
with Section VI.A.1 of the NRC Enforcement
Policy. If you contest any NCV in this report, you should provide a response within 30 days of the date of this inspection
report, with the basis for your denial, to the Nuclear Regulatory
Commission, A TIN.: Document Control Desk, Washington, DC 20555-0001;
with copies to the Regional Administrator, Region I; the Director, Office of Enforcement;
and the NRC Resident Inspector
at R.E. Ginna. In addition.
if you disagree with the characterization
of any finding in this report, you should provide a response within 30 days of the date of this inspection
report. with the basis for your disagreement, to the Regional Administrator, Region I, and the NRC Resident Inspector
at R.E. Ginna Nuclear Power Plant. The information
you provide will be considered
in accordance
with Inspection
Manual Chapter 030? In accordance
with 1 0 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure, and your response (if any) will be available
electronically
for public inspection
in the 
J. 3 NRC Public Document Room or from the Publicly Available
Records (PARS) component
of the NRC's document system (ADAMS). ADAMS is accessible
from the NRC Web Site at http://www.nrc.gov/reading-rm/adams.html(the
Public Electronic
Reading Room). Sincerely, ,/;I,/;tJ--fbr-Division of Reactor Projects Docket No.: 50-244 License No.: DPR-18
Inspection
Report 05000244/2009008
w/Attachment
A: Supplemental
Information
w/Attachment
B: Special Inspection
Charter cc w/encl: Distribution
via ListServ 
J. 2 NRC Public Document Room or from the Publicly Available
Records (PARS) component
of the NRC's document system (ADAMS). ADAMS is accessible
from the NRC Web Site at httg:llwww.nrc.gov/reading*rm/adams.html(the
Public Electronic
Reading Room). Sincerely, IRAJ James W. Clifford for: David C. lew, Director Division of Reactor Projects Docket No.: 50-244 License No.: DPR-18
Inspection
Report 05000244/2009008
w/Attachment
A: Supplemental
Information
w/Attachment
B: Special Inspection
Charter cc w/encl: Distribution
via
SUNSI Review Complete:
gtd (Reviewer's
DOCUMENT NAME: G:\DRP\BRANCH1\Ginna\TDAFW
SIT\AED Track Changes Ginna Report Rev 4 After declaring
this document "An Official Agency Record" it will be released to the To receive I!I copy of this document, indicate in the box: "C' =Copy without attachmenVenclosure "e" =Copy with attaclhmentlenclosure "N";:; No co ML093160122
RI/ENF OFFICE RI/DRS RI/DRP NAME CCahill/cc*
JClifford/jwc
DATE 10/21109 11/05/09 *see prior concurrence
OFFICIAL RECORD COpy Distribution
w/encl: S. Collins, RA (R10RAMaii
Resource)
ROPreports@nrc.gov
M. Dapas, ORA (R10RAMaii
Resource)
D. Lew, DRP (R1DRPMaii
Resource)
J. Clifford, DRP (R1DRPMail
Resource)
l. Trocine, RI OEDO RidsNrrPMREGinnaResource
RidsNrrDorlLpl1-1
Resource G. Dentel, DRP N. Perry, DRP J. Hawkins, DRP K. Kolaczyk, DRP, SRI S. Kennedy, DRP, SRI L. Casey, DRP, RI M. Rose, DRP, OA D. Bearde, DRP 
Docket License Report Team
Approved U.S. NUCLEAR REGULATORY
REGION 50-244 DPR-18 05000244/2009008
Constellation
Energy, R. E. Ginna Nuclear Power Plant, LLC R. E. Ginna Nuclear Power Plant Ontario. New York June 15-19, 2009 and August 24-27.2009
C. cahill, Senior Reactor Analyst, Division of Reactor Safety S. Kennedy, Senior Resident Inspector, Division of Reactor Projects K. Kolaczyk, Senior Resident Inspector, Division of Reactor Projects J. Bream, Project Engineer.
Division of Reactor Projects Glenn T. Dentel, Chief Projects Branch 1 Division of Reactor Projects 
2 SUMMARY OF FINDINGS IR 05000244/2009008;
06/15-19/2009
and 08/24-2'712009;
R. E. Ginna Nuclear Plant; Special Inspection
Team Report. The report covered two on-site inspection
visits and related in-office
inspection
activities
by a special inspection
team consisting
of a Senior Reactor Analyst. two Senior Resident Inspectors.
and one Project Engineer.
One apparent violation (A V) with potential
for greater than Green safety significance
and two Green findings were identified.
The significance
of most findings is indicated
by its color (Green. White, Yellow, or Red) using Inspection
Manual Chapter (lMC) 0609, "Significance
Determination
Process." Findings for which the significance
determination (SDP) process does not apply may be Green or be assigned a severity level after NRC management
review. The NRC program for overseeing
the safe operation
of commercial
nuclear power reactors is described
in NUREG-1649, "Reactor Oversight
Process," Revision 4, dated December 2006. NRC Identified
and Self-Revealing
Findings Cornerstones:
Mitigating
Systems Preliminary
White: A self-revealing
apparent violation (A V) of 10 CFR 50, Appendix B, Criterion
XVI, uCorrective
Actions," was identified
for the failure to preclude recurrence
of a signIficant
condition
adverse to quality (SCAQ) associated
with the Turbine Driven Auxiliary
Feedwater (TDAFW) pump governor control valve. Specifically, after identifying
corrosion
of the govemor control valve stem in April 2005, Ginna did not take adequate corrective
actions to preclude the recurrence
of corrosion
which led to the binding of the gave mar control valve and failure of the TDAFW pump on July 2,2009. In addition, the inspectors
concluded
that governor control valve stem binding was the likely cause of the failure of the TDAFW pump on May 26,2009. The overspeed
trip of the TDAFW pump on May 26. 2009. was originally
determined
by Ginna to be failure of the governor control system relay valve. Governor control valve stem corrosion
is a SCAQ because corrosion
of the stem can IHad to governor control valve stem binding and failure of the TDAFW pump as discussed
in NRC Information
Notice (IN) 94-66: "Overspeed
of Turbine-Driven
Pumps Caused by Governor Valve Stem Binding" and other related industry operating
experience
documents.
Immediate
corrective
actions inCluded entering this condition
in the corrective
action program (CAP). conducting
a root cause analysis (RCA). replacing
the governor control valve stem, and conducting
weekly monitoring
of the governor control valve during surveillance
testing to identify any potential
for stem binding. In addition, corrective
actions included a follow-up
inspection
of the governor control valve during the fall 2009 refueling
outage. Ginna will continue to monitor the govemor control valve under an enhanced TDAFW surveillance
program to ensure TDAFW pump operability.
The finding is more than minor because it is associated
with the equipment
performance
attribute
of the Mitigating
System cornerstone
and affects the cornerstone
objective
to ensure the availability, reliability, and capability
of systems that respond to initiating
events to prevent undesirable
consequences.
Specifically.
stem corrosion
caused binding of the governor control valve and led to the failure of the TDAFW pump. This finding was assessed using IMC 0609 and preliminarily
determined
to be White (lOW to moderate safety significance)
based on a Phase 3 analysis with a total (internal
and Enclosure 
external contributions)
calculated
conditional
core damage frequency (CCDF) of B.6E-6. This finding has a cross-cutting
aspect in the area of Problem Identification
and Resolution, Corrective
Action Program, because Ginna did not implement
a corrective
action program with a low threshold
for identifying
issues completely, accurately, and in a timely manner commensurate
with their safety significance
[P.1(a} per IMC 0305]. Specifically, Ginna did not identify issues
with corrosion
of the governor control valve within the corrective
action program. (Section 2.1.1) Green: A self-revealing
non-cited
violation (NCV) of 10 CFR 50, Appendix B, Criterion
XVI, "Corrective
Actions," was identified
for the failure to establish
adequate measures to correct a longstanding
issue associated
with steam admission
valves leakage. As a result, the leakage most likely contributed
to the build-up of corrosion
on the TDAFW pump governor control valve stem and contributed
to the failure of the TDAFW pump on May 26, 2009, and on July 2, 2009. The steam admission
valves had been leaking since at least 2005. However, G.inna did not take adequate measures to correct the leakage or minimize the impact of the leakage on governor control valve performance.
Immediate
corrective
actions included entering this condition
in the corrective
action program, conducting
a root cause analysis, replacing
the governor control valve stem, and conducting
weekly monitoring
of the governor control valve during surveillance
testing to identify any potential
for stem binding. Additionally, the steam admission
valves were inspected
and re-worked
and the governor control valve was inspected
during the fall 2009 outage. Ginna will continue to monitor the governor control valve under an enhanced TDAFW surveillance
program to ensure TDAFW pump operability.
Planned corrective
actions include
the steam admission
valves in May 2011. The finding is more than minor because it is associated
with the equipment
performance
attribute
of the Mitigating
Systems cornerstone
and affects the cornerstone
objective
to ensure the availability
and reliability
of systems that respond to initiating
events to prevent undesirable
consequences.
Specifically, leakage through the steam admission
valves can result in continuous
wetting of the governor control valve stem and lead to or accelerate
corrosion
of the governor control valve. This could result in a stem binding of the governor control valve and failure of the TDAFW pump. The inspectors
evaluated
the signifiCance
of this finding using IMC 0609, Attachment
4, "'Phase 1 -Initial Screening
and Characterization
of Findings." The finding is of very low safety significance
because it is not a design or qualification
deficiency, did not represent
a loss of a safety function of a system or a single train greater than its technical
speCification (TS) allowed outage time, and did not screen as potentially
risk Significant
due to external events. This finding has a cross-cutting
aspect in the area of Problem Identification
and Resolution, Corrective
Action Program, because Ginna did not thoroughly
evaluate problems such that the resolutions
address causes and extent of conditions, as necessary, In a timely manner, commensurate
with their significance
[P.1 (c) per IMC 0305]. Specifically, Ginna did not thoroughly
evaluate the potential
effect of the steam admission
valve leakage on the governor control valve performance. (Section 2.1.2) Green: The inspectors
identified
an NCVof 10 CFR 50, Appendix B. Criterion
III, "Design Control," for the failure to establish
measures to ensure that a modification
performed
on the governor control valve bushing was a suitable application
of materials
for the TDAFW pump. During a review of the RCA associated
with the TDAFW pump failures, the inspectors
noted that Ginna did not consider the potential
impact of Enclosure 
removing some of the hardened layer of the bushing on the corrosion
rate of the governor control valve. Following
concerns raised by the inspectors, Ginna inspected
the governor control valve bushing during the fall 2009 refueling
outage and observed corrosion
of the bushings.
Ginna noted that the corrosion
of the bushings appeared to have been caused by the lapping of the bushing to achieve the increased
clearance
between the stem and the bushings.
Immediate
corrective
actions following
the inspection
of the governor control valve during the fall 2009 refueling
outage included entering this condition
in the CAP and refurbishing
the governor control valve with a new stem and bushing. The finding is more than minor because it is associated
with the equipment
performance
attribute
of the Mitigating
System cornerstone
and affects the cornerstone
objective
to ensure the availability, reliability, and capability
of systems that respond to initiating
events to prevent undesirable
consequences.
Specifically, lapping of the valve bushing resulted in an unanticipated
corrosion
mechanism
of the govemor control valve that impacted the reliability
of the TDAFW pump" The inspectors
evaluated
the significance
of this finding using IMC 0609, Attachment
4. "Phase 1 Initial Screening
and Characterization
of Findings." The finding is of very low safety significance
because it is a design or qualification
deficiency confirmed not
to result in the loss of operability
or functionality.
The inspectors
determined
that this finding has a cross-cutting
aspect in the area of Human Performance, Decision Making. because Ginna did not make a safety-significant
or risk-significant
decision using a systematic
process, especially
when faced with uncertain
or unexpected
plant conditions, to ensure safety was maintained
[H.1(a) per IMC 0305]. Specifically, Ginna did not use a systematic
process such as an engineering
evaluation
to properly evaluate the potential
impact of removing some of the hardened layer of the bushing. [H.1 (a) per IMC 0305] (Section 2.3) Licensee Identified
Violations
None Enclosure 
REPORT DETAILS 1. INTRODUCTION
1.1 Background
and Event Description
On May 26, 2009, and July 2, 2009, the TDAFW pump tripped on overspeed
during the performance
of surveillance
testing activities.
These were the second and third times the TDAFW pump had failed a surveillance
test in a six month period. The previous test failure occurred on December 2, 2008, when the TDAFW pump failed to develop acceptable
discharge
pressure during a quarterly
surveillance
test. Details surrounding
the December test failure including
Ginna corrective
actions are discussed
in NRC Integrated
Inspection
Report 50-244/2009002.
Following
each of the three test failures, Ginna declared the TDAFW pump inoperable
and entered the limiting Condition
for Operation
for TS 3.7.5 "Auxiliary
Feedwater." Following
the May 26, 2009, test failure, Ginna troubleshooting
activities
were focused on the TDAFW lubricating
oil system where system pressure oscillations
were noted by test personnel
prior to the pump overspeed
trip. As part of the troubleshooting
efforts, the TDAFW lubricating
oil system was drained and refilled with fresh oil, filters in the lubrication
system were examined and replaced, and several components
in the lubricating
oil system including
the relay and pressure regulating
valves were replaced.
Additionally
the turbine governor linkage was adjusted to original specifications
outlined in the vendor technical
documents.
Although several out of speCification
and missing components
were identified
during this troubleshooting
effort, a definitive
cause for the surveillance
failure was not identified.
Nevertheless, following
the successful
completion
of post maintenance
testing activities, Ginna declared the TDAFW pump operable and commenced
an augmented
surveillance
testing program for the TDAFW pump that tested the pump on a weekly basis. On July 2, 2009, another TDAFW pump overspeed
failure occurred when the pump was undergoing
the augmented
testing program. Troubleshooting
activities
following
this failure were focused on the turbine control system, which did not appear to have functioned
properly during the test. Accordingly, the turbine control and relay valves were disassembled
and inspected, and the governor linkage system was adjusted.
Additionally.
the lubricating
oil system was flushed and examined for particulates.
However, unlike the May 26 failure, these troubleshooting
activities
identified
a definitive
cause, a stuck governor control valve stem, that resulted in the surveillance
test failure. Visual inspection
of the stem, which had become bound to its bushing and had to be forcibly removed, revealed corrosion
buildup where the stem contacted
the upper valve bushing. To restore the control valve to an operable status, Ginna replaced the valve stem and increased
the bushing clearances
to dimensions
specified
by the Ginna TDAFW pump inspection
procedure.
The pump was successfully
tested and declared operable subject to an augmented
testing program. Ginna assigned an RCA team to investigate
the surveillance
test failures.
The Ginna RCA team concluded
that the primary root cause of the failure of the governor contrOl valve to control turbine speed on July 2,2009, was binding caused by a corrosion
mechanism
that occurred between the valve stem and the valve bushings.
The RCA team also concluded
that stem binding appeared to be an intermittent
problem and that Enclosure 
station members missed opportunities
to identify the failure mode during previous surveillances
and failures.
As such, the RCA team determined
that governor control valve stem binding could not be ruled out as a possible failure mode during the December 2008 and the May 2009 TDAFW pump failures.
At Ginna's request, an independent
vendor reviewed the issues associated
with the governor control valve stem binding to determine
the failure mechanism
that was the cause of the TDAFW pump overspeed
trips. The vendor determined
that the most likely cause of the corrosion
of the governor control valve stem was fresh-water
corrosion (Langelier
corrosion)
that was the result of galvanic interactions
between the nitrided case and the base material of the governor control valve stem. The vendor considered
several variables
that contributed
to the corrosion
mechanism
such as material composition
of the stem and bushing, stem-to-bushing
clearance, steam admission
valve leakage, and TDAFW pump surveillance
frequency
and duration.
1.2 Special Inspection
Scope The NRC conducted
this inspection
to gain a better understanding
of the circumstances
involving
the TDAFW pump overspeed
trips during surveillance
testing on May 26, 2009, and on July 2,2009. The inspection
team used NRC Inspection
Procedure
93812, "Special Inspection," as a guide to complete their review. Additional
inspection
and review activities
were outlined in the special inspection
team charter, provided as Attachment
B. The special inspection
team reviewed procedures, corrective
action documents, work orders, engineering
analyses, and the root cause evaluation
prepared by Ginna. In addition.
the team conducted
equipment
walkdowns
and interviewed
key plant personnel
regarding
the discovery
and resolution
of the condition.
A list of site personnel
interviewed
and documents
reviewed are provided in Attachment
A to this report. 1.3 Preliminary
Conditional
Risk Assessment
Using IMC 0309, "Reactive
Inspection
Decision Basis for Reactors," IMe 0609, "Significance
Determination
Process," and the Ginna Standardized
Plant Analysis Risk (SPAR) model in conjunction
with the Graphical
Evaluation
Module (GEM). the Region I Senior Reactor Analyst (SRA) evaluated
the increase in conditional
core damage probability
for the failure of the TDAFW pump. Based on the nature of the failure and the subsequent
overspeed
trip on an instrumented
diagnostic
run, the condition
was evaluated
as being non-recoverable
in the event of actual demand. Based upon best available
information, an incremental
conditional
core damage probability (ICCDP) in the upper E-6 range (8E-6 per the 82 day exposure period), was calculated.
The exposure period was based on the assumption
that the TDAFW pump would not have started since the last time it passed a surveillance
test on March 5 until May 26 (82 days). The dominant core damage sequence was a station blackout (loss of offsite power (LOOP) with failure of both emergency
diesel generators (EDGs), with no TOAFW and failure to recover offsite power or an EDG in one hour. Based upon this conservative
conditional
core damage probability (CCDP) value, and having satisfied
an IMC 0309 deterministic
criterion, the May 26 degraded TDAFW pump Enclosure 
condition
fell within the Special Inspection
to Augmented
Inspection
Team range for reactive inspections.
2. SPECIAL INSPECl"ION
AREAS 2.1 Review of Maintenance
a. Inspection
Scope The team evaluated
the adequacy and completeness
of the maintenance
on the TDAFW system, including
preventive
maintenance, procedural
guidance, post-maintenance
testing, and supervisory
oversight.
The team independently
evaluated
selected procedures, preventive
maintenance
strategies.
condition
reports (CRs). system health reports. and associated
work orders. In addition, the team reviewed the RCA, conducted
equipment
walkdowns
and interviewed
key station personnel.
For the weaknesses
identified, the inspectors
verified that appropriate
corrective
actions have been planned or taken. b. Findings and Observations
1. Failure to Preclude Recurrence
of a Significant
Condition
Adverse to Quality Introduction:
A self-revealing
AV of 10 CFR 50, Appendix S, Criterion
XVI, "Corrective
Actions," was identified
for the failure to preclude recurrence
of a SCAQ associated
with the TDAFW pump governor control valve. Specifically, after identifying
corrosion
of the governor control valve stem in April 2005, Ginna did not take adequate corrective
actions to preclude the recurrence
of corrosion
which led to the binding of the governor control valve and failure of the TDAFW pump on July 2, 2009. In addition, governor control valve stem binding was a fikely failure of the May 26, 2009, TDAFW pump overspeed
trip. This finding was preliminarily
determined
to be White. Description:
On April 11, 2005, Glnna conducted
a periodic major inspection
of the TDAFW pump governor control valve under work order #20401907.
During the disassembly
of the valve, mechanics
noted corrosion
in the bushing area of the stem plug. The vendor recommended
replacing
the valve stem and plug due to the corrosion.
However, Ginna did not recognize
stem corrosion
as a condition
adverse to quality and did not initiate a CR in accordance
with station guidance in IP-CAP-1 r "Condition
Reporting." As a result, Ginna did not conduct any further analysis or evaluation
to determine
the cause of the corrosion.
On July 2, 2009, during surveillance
testing, the TDAFW pump tripped due to overspeed. Ginna
formed an Issue Response Team and developed
a comprehensive
troubleshooting
plan to determine
the cause(s) of the failure. The troubleshooting
plan consisted
of all possible failure modes, possible causes of each failure mode, and actions to validate or refute each "failure mode. Upon disassembly
of the governor control valve, the stem was found seized within its bushings and had to be forcibly removed. Visual inspection
showed pitting on the surface of the stem Where it contacted
the upper valve bushing. Following
completion
of the troubleshooting
activities, Ginnaconcluded
that TDAFW pump failure was due to binding of the governor control valve and that the binding was caused by the build up of corrosion
on the valve stem. Enclosure 
Governor control valve stem corrosion
is an SCAQ because corrosion
of the stem can lead to govemor control valve stem binding and failure of the TDAFW pump as discussed
in NRC IN 94-66: "Overspeed
of Turbine-Driven
Pumps caused by Governor Valve Stem Binding," and other related industry operating
experience
documents.
Immediate
corrective
actions included entering this condition
in the CAP, conducting
an RCA, replacing
the governor control valve stem, and conducting
weekly monitoring
of the governor control valve during surveillance
testing to identify any potential
for stem binding. In addition, corrective
actions included a follow-up
inspection
of the governor control valve during the fall 2009 refueling
outage. Because additional
corrosion
was found during this inspection
on September
18, 2009, the control valve was sent to the vendor to be refurbished.
Ginna will continue to monitor the governor control valve under an enhanced TDAFW surveillance
program to ensure TDAFW pump operability.
Ginna also was evaluating
longer term corrective
actions to address the corrosion
including
more frequent governor control valve stem replacement, change of the stem material, and other modifications
to the system design. Planned corrective
actions include replacing
the stem admission
valves in May 2011. The inspectors
noted that governor control valve stem binding also could have been a contributor
to the December 2, 2008, TDAFW pump failure to develop the minimum acceptable
discharge
flow and pressure, and the likely cause of the May 26, 2009, TDAFW pump overspeed
trip. Following
these events, Ginna missed opportunities
to identify potential
stem binding problems after identifying
possible indicators
of this failure mode such as leaking steam admission
valves and rust/corrosion
on the visible portion of the governor valve stem. In addition, during troubleshooting
efforts in May 2009, . Ginna missed an opportunity
to exercise the governor control valve stem with the linkage disconnected
and lube oil pressure not applied. Operating
experience
suggested
that cycling the valve by hand without hydraulics
applied is a prudent action to validate or refute governor control valve stem binding. Analysis:
The performance
deficiency
is that Ginna did not take adequate measures to correct a condition
that had the potential
to impact the operability
of the TDAFW pump. Specifically, after identifying
corrosion
on the governor control valve stem in 2005, Ginna did not take adequate corrective
actions to preclude the recurrence
of corrosion
which led to the binding of the governor control valve and failure of the TDAFW pump. The finding is more than minor because it is associated
with the equipment
performance
attribute
of the Mitigating
System cornerstone
and affects the cornerstone
objective
to ensure the availability, reliability, and capability
of systems that respond to initiating
events to prevent undesirable
consequences.
Specifically, stem corrosion
caused binding of the governor control valve and led to the failure of the TDAFW pump. In accordance
with IMe 0609, Attachment
4, "Phase 1 -Initial Screening
and Characterization
of Findings," a Phase 2 risk analysis was required because the finding represents
an actual loss of safety function of a single train for greater than the TS allowed outage time of 7 days. The Phase 2 risk evaluation
was performed
in accordance
with IMC 0609, Appendix A, Attachment
1, "User Guidance for Phase 2 and Phase 3 Reactor Inspection
Findings for At*,power
Situations." Because the precise time is unknown for the inception
of TDAFW pump inoperability, an exposure time of one-half of the time period (t/2) between discovery (May 26, 2009) to the last successfully
completed
quarterly
surveHlance
test (March 5, 2009) was used. This t/2 exposure time Enclosure 
9 equals 51 days. Using Ginna's Phase 2 SDP notebook, pre-solved
worksheets, and an initiating
event likelihood
of 1 year (>30-days
exposure time), the inspector
identified
that this finding is of potentially
substantial
safety significance (Yellow).
The dominant sequence identified
in the Phase 2 notebook involves a loss of offsite power (LOOP), failure of both EDGs, and the subsequent
loss of the TDAFW pump, with the failure of operators
to restore offsite power within 1 hour: LOOP (2) + EAC (3) + TDAFW (0) + REC1 (0) = 5 (Yellow).
In recognition
that the Phase 2 notebook typically
yields a conservative result, a
NRC Region I Senior Reactor Analyst (SRA) performed
a Phase 3 risk assessment
of this finding. The SRA used Ginna's Standardized
Plant Analysis Risk (SPAR) model, Revision 3.45, dated June 2008. and graphical
evaluation
module, in conjunction
with the System Analysis Programs for Hands-On Integrated
Reliability
Evaluations (SAPHIRE).
Version 7, to estimate the internal risk contribution
of the Phase 3 risk assessment.
The following
assumptions
were used for this assessment: Based on the guidance provided in the Risk Assessment
of Operational
Events Handbook, Revision 1.01, the calculated
exposure was determined
to be 1198 hrs. The summation
of this exposeure
time was determined
as follows: One half the exposure time, (tI2), was applied for the period between March 5 -May 26, 2009 The full exposure time, (t). was applied for the unavailability
and troubleshooting
from May 26 -May 29, 2009. One half the exposure time. (tI2), was applied for the period between June 25 -July 2, 2009 The full exposure time, (t), was applied for the unavailability
and troubleshooting
from July 2 -July 5, 2009 To closely approximate
the type of f*lilure exhibited
by the TDAFW pump, the fail to start basic event <AFW-TDP-FS-TDP>
was changed from its baseline failure probability
to 1.0, representing
a 100 percent failure to start condition. Based on the nature of the failure. and no recovery procedures
in place, there was no recovery credit assigned to the May failure. The loss of service water initiating
event frequency (IE-LOSWS)
was increased
from its nominal value of 4.0E-4 to 2.0E*3 to more closely model the risk of a LOSWS at the Ginna station. This is consistent
with Ginna's understanding
of the risk of this event. All remaining
events were left at their nominal failure probabilities. The model was modified by Idaho National Laboratory (INL) to include convolution
correction
factors. Convolving
the failure distribution
eliminates
the simplifying
assumption
that all failure to run events happen at time=O. Inclusion
of this correction
can reduce station blackout (SBO) core damage frequency (CDF) significantly
for plants like Ginna that have low EDG redundancy. Since all observed failures happened upon the initiation
of the TDAFW system, the period between May 29 and June 25 2009, was not included in the exposure period because the system successfully
completed
increased, weekly, surveillance
testing. The team could not conclude that the stem binding condition
would occur after the pump had been successfully
started and run. Cutset probability
calculation
truncation
was set at 1 E-13. Enclosure 
Based upon the above assumptions, the Ginna SPAR model calculated
an increase in internal event contribution
to conditional
core damage probability (CCDP) of 2.9E-6. This low-ta-mid
E-6 delta CCDP value represents
a low to moderate safety significance (White). The dominant internal event sequence involved a LOOP with subsequent
failure of the EDGs (station blackout event), the failure of the TDAFW train and the failure to recover AC power. The Phase 3 SPAR model results correlate
well to the Phase 2 SDP Notebook dominant core damage sequences.
External Events Risk Contribution
The Ginna Probablistic
Safety Assessment (PSA) includes a Level 1 analysis of fires and flooding external events. The PSA summarizes
the fire contribution
as representing
approximately
48% of the total (internal
and external)
core damage frequency, or nearly half of the annualized
risk. The NRC does not have an external event risk model for Ginna. Consequently, the SRA, after review of the licensee's
Individual
Plant Examination
of External Events (IPEEE), utilized the licensee's
external events assessment
to quantify the fire and flooding events risk contribution
for this condition.
Seismic event likelihood
was considered
to be very low and determined
not to be a significant
contributor
to the risk of this condition.
The results of the PSA for this condition
calculated
a CCDP contribution
from fire events at 5E-6 and from flooding at 7E-7. The most significant
fire initiated
core damage sequence involved a spectrum of control room fires, with a failure of automatic
and manual suppression, a failure of the TDAFW pump and a failure of the 'C' standby auxiliary
feed water pump for decay heat removal via the steam generators.
The most Significant
flooding core damage sequence quantified
in the PSA for this condition, Involved flooding in the relay room, failure of the TDAFW pump and a failure to align standby auxiliary
feed water pump for decay heat removal via the steam generators.
Large Early Release Frequency (LERF) Evaluation
The SRA used IMC 0609, Appendix H, "Containment
Integrity
Significance
Determination
Process," to determine
if this finding was a significant
contributor
to a large early release. The Ginna containment
is classified
as a pressurized
water reactor large-dry
containment
deSign. Based upon the dominant sequences
involving
LOOP and station blackout (S80) initiating
events, per Appendix H, Table 5.2, "Phase 2 Assessment
Factors -Type A Findings at Full Power," the failure of the TDAFW pump does not represent
a significant
challenge
to containment
integrity
early in the postUlated
core damage sequences.
Consequently, this finding does not screen as a significant
large early release contributor
because the close-in populations
can be effectively
evacuated
far in advance of any postulated
release due to core damage, Accordingly, the risk significance
of this finding is associated
with the delta CDF value, per IMC 0609, Appendix H, Figure 5.1, and not delta LERF. Risk Assessment
Summary The calculated
total risk significance
of this finding is based upon the summation
of internal and external risk contributions (delta CCDP internal + delta CCDP external (fires and floods).=
delta CCDP total). 2.9E-6 + 5E-6 + 7E-7 = 8.6E-6 delta ceDP. Enclosure 
Annualized, this value of 8.6E-6 delta CDF represents
a low to moderate safety significance
or White finding. Licensee's
Risk Assessment
Summary Constellation's
risk assessment
for the given condition, assuming no operator recovery, resulted in a total delta CDF value of 1.028E-5.
This increase in CDF value comprised
of: 4.6E-6 due to intemal events; 0.7E-6 due to intemal flooding events; and 5E-6 fire/external
events. Similar to the NRC internal risk contribution, the largest percentage
of intemal risk was derived from station blackout events. The licensee conducted
refinements
in their modeling to credit additional
recovery options in the event that the TDAFW pump failed. By crediting
these recovery actions, the delta CDF was reduced from 1.028E-5 to 9.2 E-6, or by approximately
10%. The specific recovery actions are as follows: . The potential
for operators
to use standby auxiliary
feedwater (SAFW) pump C, in lieu of the TDAFW pump during fire and flood scenarios
which require use of alternate
shutdown procedures
was modeled. Although use of an SAFW pump is not specifically
called out in these procedures, the procedures
do explicitly
recognize
that if the TDAFW pump is not functioning, a loss of secondary
heat sink will result, and direct operators
to refer to other emergency procedures
for alternate
methods of establishing
a heat sink (see ER-FIRE.1
step 4.3.4.2, FIRE.2 step 4.3.12, etc.}. In response to this hypothetical
scenario, an operations
Shift Manager (SM) indicated
that upon a failure of the TDAFW to provide flow, a SAFW pump could be manually started by locally opening the service water suction valve to the pump and locally closing the breaker to the pump motor. The steps necessary
to align an SAFW pump to the steam generators (SG) are contained
in emergency
operating
procedures (EOP) Attachment
5.1 'Attachment
SAFW'. Since only Busses 14 and 18 are energized
during ER-FIRE scenarios, SAFW pump C would be used. Following
the May 26th overs peed trip of the TDAFW pump, new section 2.2 was added to procedure
P-15.6, 'Operation
of the TDAFW Pump Trip Throttle Valve.' Revision 00200. This step provides instructions
for a 'slow start' of the TDAFW pump manually, following
an overspeed
trip of the pump, by using the trip throttle valve. This allows for starting of the pump even if the governor control valve is stuck in the full open position following
the overspeed
trip. This procedure
step was successfully
used following
both the May 26th failure and the July 2nd failure. Per Operations
management, the shift managers, who would be directing
use of this procedure, were briefed on the updated procedure
to ensure they were aware that new step was available
for use and understood
how it was to be performed.
A controlled
copy of the procedure
is located at the TDAFW pump for use by the operator.
Since this procedure
was in effect prior to the July failure exposure period (Le., prior to the last successful
TDAFW pump test on June 25, 2009), it is considered
as a recovery for failures of the TDAFW pump. Recovery actions identified
in #1 above were not quantified
by the team however the evaluation
approach appears to be appropriate.
Prior to the licensee crediting
recovery actions identified
in #2 above, the team was able to verify that the procedures
were in Enclosure 
place and observed troubleshooting
video in which the licensee started the TDAFW pump with this method. As a result the SRA concluded
that the licensee's
modeling demonstrating
a risk reduction
was appropriate.
Based upon the close comparison
between NRC and Constellation
risk estimates, no sensitivity
analyses were warranted.
The use of V2 to approximate
the exposure time was determined
to be appropriate
for standby or periodically
operated components
that fail due to a degradation
mechanism
that gradually
affects the component
during the standby time period. Inclusion
of the unavailability
time hours, due to troubleshooting
and repairs, is also appropriate
and consistent
with the guidance promulgated
in Risk Assessment
of Operational
Events Handbook, Revision 1.01, dated January 2008. This finding has a cross-cutting
aspect in the area of Problem Identification
and Resolution, Corrective Action Program, because Ginna did not implement
a corrective
action program with a low threshold
for identifying
issues completely, accurately, and in a timely manner commensurate
with their safety
significance.
Specifically, Ginna did not identify issues associated
with corrosion
of the governor control valve within the corrective
actions program. The inspectors
concluded
that the performance
deficiency
is reflective
of current performance
because Ginna had reasonable
opportunities
to identify the issue during troubleshooting
in December 2008 and May 2009. [P.1(a) per IMC 0305] Enforcement:
10 CFR 50, Appendix B, Criterion
XVI, "Corrective
Actions," states, in part, "Measures
shall be established
to assure that conditions
adverse to quality, such as failures, malfunctions, defiCiencies, deviations, defective
material and eqUipment, and nonconformances
are promptly identified
and corrected.
In the case of significant
conditions
adverse to quality, the measures shall assure that the cause of the condition
is determined
and corrective
action taken to preclude repetition." Contrary to the above, after identifying
corrosion
on the TDAFW pump governor control valve stem on April 11, 2005, which is a significant
condition
adverse to quality, Ginna did not take adequate measures to determine
the cause and prevent recurrence.
The cause of the condition
was left uncorrected
and resulted in additional
stem corrosion
that led to binding of the governor control valve and the failure of the TDAFW pump on July 2, 2009. In addition, stem corrosion
was the likely cause of the TDAFW pump failure on May 26, 2009. This issue was entered into Ginna's CAP as CR-:2009-003680
and CR-2009-004577.
Pending final determination
of significance, this finding is identified
as an AV. (AV 0500024412009008*01:
Inadequate
Corrective
Actions Associated
with the TDAFW Pump Governor Control Valve) 2. Untimely Corrective
Actions Associated
with Steam Admission
Valves Introduction:
A self-revealing
NeVof 10 CFR 50, Appendix B, Criterion
XVI, "Corrective
Actions," was identified
for the failure to establish
adequate measures to correct a longstanding
issue associated
with steam a(]mission
valves leakage. As a result, the leakage most likely contributed
to the build-up of corrosion
on the TDAFW pump governor control valve stem on May 26, 2009 and contributed
to the failure of the TDAFW pump on July 2, 2009. Description:
During a review of failures associated
with the TDAFW pump, the inspectors
noted that the steam admission
valves had a history of leaking. Based on a review of the RCA report, industry operating
experience, and associated
CRs, the Enclosure 
inspectors
determined
that the steam admission
valve leakage was a contributing
factor in the development
of corrosion
of the governor control valve and contributed
to the failure of the TDAFW pump on July 2, 2009, and most likely the failure of the TDAFW pump overspeed
trip failure on May 26, 2009. Based on a review of eRs and interviews
of personnel, the inspectors
determined
that the steam admission
valves had been leaking since at least 2005. In July 2005,
documented
that steam admission
valve 3505A was leaking past its seat. However, Ginna did not take or plan any corrective
actions associated
with the issue. By October 2006, steam admission
valve 3505A leakage had increased
such that the TDAFW pump turbine was rotating approximately
100 rpm. Ginna cycled the valve to reduce seat leakage, generated
a work order to repair the valve in May 2008, and conducted
an evaluation
of past operability.
Ginna concluded
that there was no potential
for increased
consequences
with time if the condition
continued.
During the May 2008 refueling
outage, Ginna conducted
a repair of steam admission
valve 3505A. However, this corrective
action was not effective;
by September
2008, the valve was leaking again although at a reduced rate. The inspectors
determined
that Ginna did not recognize
or consider the potential
impact of the steam admission
valve leakage on the governor control valve stem. Immediate
corrective
actions included entering this condition
in the CAP, replacing
the govemor control valve stem, and conducting
weekly monitOring
of the governor control valve during surveillance
to identify any potential
for stem binding. Additionally, the steam admission
valves were inspected
and re-worked
and the govemor control valve was Inspected
during the fall 2009 outage. Ginna will continue to monitor the governor control valve under an enhanced TDAFW surveillance
program to ensure TDAFW pump operability.
Planned corrective
actions include replacing
the stem admission
valves in May 2011. Analysis:
The performance
deficiency
is that Ginna did not adequately
address deficiencies
associated
with steam admission
valve leakage in that the leakage likely resulted in accelerated
corrosion
of the governor control valve and contributed
to the failure of the TDAFW pump. The finding is more than minor because it is associated
with the equipment
performance
attribute
of the Mitigating
Systems cornerstone
and affects the cornerstone
objective
to ensure the availability
and reliability
of systems that respond to initiating
events to prevent undesirable
consequences.
Specifically, leakage through the steam admission
valves can res.ult in continuous
wetting of the governor control valve stem and lead to or accelerate
corrosion
of the governor control valve. This could result in a stem binding of the govemor control valve and failure of the TDAFW pump. The inspectors
evaluated
the significance
of this finding using IMC 0609, Attachment
4, "Phase 1 -Initial Screening
and Characterization
of Findings." The finding is of very low safety significance
because it is not a design or qualification
deficiency, did not represent
a loss of a safety function of a system or a single train greater than its TS allowed outage time, and did not screen as potentially
risk Significant
due to external events. The inspectors
determined
that the steam admission
valve leakage was not a direct cause of the failure of the TDAFW pump overspeed
events. The steam admission
valve leakage was a contributing
factor in the development
of governor control valve stem corrosion
and contributed
to the failure of the TDAFW pump. Enclosure 
This finding has a cross-cutting
aspect in the area of Problem Identification Resolution, Corrective
Action Program, because Ginna did not thoroughly
problems such that the resolutions
address causes and extent of conditions, r:eecessary, in a timely manner, commensurate
with their significance.
Ginna did not thoroughly
evaluate the potential
effect of the steam admission leakage on the governor control valve performance.
The inspectors
determined
that issue is reflective
of current licensee performance
because each time the issue identified
and a CR was generated
represented
an opportunity
for Ginna to
evaluate the issue and assign appropriate
corrective
actions. [P.1 (c) per IMC Enforcement:
10 CFR Part 50, Appendix B, Criterion
XVI, "Corrective
Actions," states, in part. "Measures
shall be established
to assure that conditions
adverse to quality, such as failures, malfunctions, deficiencies, deviations, defective
material and equipment, and nonconformances
are promptly identified
and corrected." Contrary to this requirement, from at least July 2005 to July 2, 2009, Ginna did not established
adequate measures to correct longstanding
steam admission
valves leakage and/or minimize the impact of the leakage on the TDAFW pump governor control valve performance.
As a result, leakage I*I through the steam admission
valves contributed
to the corrosion
of the governor valve and contributed
to the failure of the TDAFW pump on July 2, 2009 and most the failure of the TDAFW pump on May 26, 2009. Because this violation
is of very safety significance (Green) and Ginna entered this issue into their CAP for resolution CR-2009-003680
and CR-2009-004577, this violation
is being treated as an consistent
with the NRC Enforcement
Policy. (NCV 0500024412009008-02:
Corrective
Actions Associated
with Stearn Admission
Valve
2.2 Review of Operating
Experience
a. Inspection
ScoQe The team reviewed operating
experience
involving
TDAFW pump failures and taken by the Ginna staff to identify and address these types of failures.
In addition, team examined the specific issues associated
with governor control valve stem to assess any new generic issues of industry interest for prompt communication dissemination.
As part of this evaluation, the inspectors
reviewed pertinent
operating
experience, Ginna's response to NRC Information
Notices, and
key plant
b. Findings and Observations
No Findings of Significance
Identified.
The inspectors
determined
that there were no new generic issues identified
as a result of this event. However, the inspectors
noted that Ginna missed opportunities
to utilize industry operating
experience
to identify precursors
associated
with this event and to conduct effective
troubleshooting.
Specifically, following
the discovery
of corrosion
on the exposed portion of the TDAFW pump govemor control valve stem in May 2005, Ginna did not enter this issue in to their CAP. As a result Ginna missed an opportunity
to revisit operating
experience
from NRC IN 94-66 conceming
governor control valve stem binding. In several examples in NRC IN 94-66, sites that experienced
governor control valves stem binding identified
stem corrosion
following
valve disassembly.
Ginna Enclosure 
had originally
determined
that NRC IN 94-66 was not applicable
to Ginna because the governor control valve was of a different
configuration
and material as those discussed
in the IN and that corrosion
of the stem had not been previously
identified.
Although this may have been a reasonable
assessment
during the original review of the NRC IN 94-66 in 1994, the inspectors
determined
that once corrosion
of the stem was identified
in'May 2005, Ginna missed an opportunity
to revisit this operating
experience.
In addition, as discussed
in Section 2.1.2 of this report. Ginna did not utilize Industry operating
experience
in evaluating
a condition
associated
with steam admission
valve leakage. NRC IN 94-66, other industry operating
experience, and the vendor technical
manual stated that steam admission
valve leakage is a cause related to governor control valve stem binding. However, Ginna did not consider the impact of steam admission
valve leakage on the governor control valve performance.
Finally, the inspectors
noted that Ginna missed opportunities
to incorporate
industry operating
experience
during troubleshooting
efforts during the May 2009 TDAFW pump failure. NRC IN 94-66 discussed
several examples where a freedom of motion test was performed
to test for stem binding with the governor control valve linkage disconnected
and hydraulics
not applied. However, during the May 2009 event, Ginna missed an opportunity
to conduct this test and consequently, missed an opportunity
to potentially
identify the failure mode prior to the July 2, 2009, overspeed
trip. Ginna captured these issues in their CAP under CR-2009-003680
and CR-2009-004577
.. 2.3 Review of Root Cause and Extent-ot-Condition
a. Inspection
Scope The team evaluated
the adequacy of Ginna's RCA and completed
interim corrective
actions. In addition the team evaluated
the adequacy of Ginna's initial extent of condition
for the TDAFW pump failures.
The team reviewed plant drawings, procedures, and associated
system modifications.
In addition, the team conducted
a walkdown of the TDAFW system and interviewed
key Ginna personnel.
b. Findings and Observations
Introduction:
The inspectors
identified
an NCV of 10 CFR 50, Appendix B, Criterion
III, "Design Control," for the failure to establish
measures to ensure that a modification
performed
on the governor control valve bushing was a suitable application
of materials
for the TDAFW pump. Description:
During the troubleshooting
and repair of the TDAFW pump in July 2009, Ginna incorrectly
evaluated
that a vendor service bulletin allowed for larger bushing clearance
than was prescribed
in their current technical
documents.
Since there was overlap between the station technical
information
and the vendor service bulletin, Ginna decided to increase the clearance, by lapping the bushings, to reduce the likelihood
that corrosion
products would cause the stem to bind. To increase the clearance, Ginna removed some of the hardened layer on the bushing. During a review of the RCA, the inspectors
determined
that Ginna did not consider the potential
impact of removing some ot the hardened layer on the corrosion
rate of the governor control valve. The inspectors
noted that by removing some of the hardened layer, the material property of the bushing could have been changed and/or additional
micro-cracks
could have been created or exposed that could increase the corrosion
rate or potentially
cause other Enclosure 
problems such as
galling. The inspectors
noted that if the corrosion
rate is greater than predicted, then planned corrective
actions may not be adequate to maintain the TDAFW pump operable.
Additionally, the team was concerned, that by increasing
the stem to bushing clearances, the stem would be susceptible
to larger steam exposure and that this could further accelerate
the corrosion.
Following
concerns raised by the inspectors, Ginna initiated
CR-2009-005959
to ensure that all possible consequences
of lapping the TDAFW pump control valve bushing were fully evaluated.
In addition, Ginna assigned corrective
actions to inspect the control valve bushing during the fall 2009 refueling
outage. During performance
of the refueling
inspection
under WO C90623685, pitting of the stem and corrosion
of the bushings were observed.
Constellation
initiated
and noted that the corrosion
of the bushings appeared to have been caused by the lapping of the bushing to achieve the desired clearance
between the stem and the bushings.
The development
of corrosion
on the bushing reduced the margin that was predicted
to ensure adequate stem movement.
Immediate
corrective
actions following
the inspection
of the governor control valve during the fall 2009 refueling
outage included entering this condition
in the CAP and refurbishing
the governor control valve with a new stem and bushing. Analysis:
The performance
deficiency
is that Ginna failed to establish
measures to ensure that a modification
performed
on the governor control valve bushing was a suitable application
of materials
for the TDAFW pump. The finding is more than minor because it is associated
with the equipment
performance
attribute
of the Mitigating
Systems cornerstone
and affects the cornerstone
objective
to ensure the availability
and reliability
of systems that respond to initiating
events to prevent undesirable
consequences.
Specifically, lapping of the valve bushing resulted in an unanticipated
corrosion
mechanism
of the governor control valve that impacted the reliability
of the TDAFW pump. The inspectors
evaluated
the Significance
of this finding using IMC 0609, Attachment
4, "Phase 1 -Initial Screening
and Characterization
of Findings." The finding is of very low safety significance
because it is not a design or qualification
deficiency, did not represent
a loss of a safety fUnction of a system or a single train greater than its TS allowed outage time, and did not screen as potentially
risk significant
due to external events. The inspectors
determined
that this finding has a cross-cutting
aspect in the area of Human Performance, Decision Making, because Ginna did not make a safety-significant
or risk-significant
decision using a systematic
process, especially
when faced with uncertain
or unexpected
plant conditions, to ensure safety was maintained.
Specifically, Ginna did not use a systematic
process such as an engineering
evaluation
to properly evaluate the potential
impact of removing some of the hardened layer of the bushing. [H.1(a) per IMC 0305] Enforcement: 10
CFR 50, Appendix B, Criterion
III, "Design Control" states, in part, "Measures
shall also be established
for the selection
and review for suitability
of application
of materials, parts, equipment, and processes
that are essential
to the related functions
of the structures, systems and components." Contrary to the requirements, in July 2009, Ginna failed to establish
measures to ensure that a modification
performed
on the governor control valve bushing was a suitable application
of materials
for the TDAFW pump. Specifically, lapping of the valve bushing resulted in an unanticipated
corrosion
mechanism
of the governor control valve that had the Enclosure 
potential
to impact the performance
of the TDAFW pump if not corrected.
Because this violation
is of very low safety significance (Green) and Ginna entered this issue into their CAP for resolution
as CR-2009-006765, this violation
is being treated as an NCV consistent
with the NRC Enforcement
Policy. (NeV 05000244/2009008-03:
Failure To Establish
Design Control Measures Associated
With The Turbine Driven Auxiliary
Feedwater
Pump Governor Control Valve) 2.4 Risk Assessment
of the As-Found Condition
a. Insoection
Scope Prior to the initiation
of the Special Inspection
Team, the Region I SRA performed
a CCDP assessment
which conservatively
bounded the potential
risk significance
of the degraded condition, assuming the TDAFW pump would fail to star on demand to mitigate the consequences
of an event. The initial CCDP estimate was performed
in accordance
with IMC 0309, "Reactive
Inspection
Decision Basis for Reactors." The SRA used the Ginna SPAR model and associated
GEM to evaluate the potential
risk significance
of this condition.
The results of the IMC 0309 assessment
are documented
in report section 2.1.b.1 above. b. Final Risk Estimate Following
team review and independent
verification
of the degraded turbine driven auxiliary
feed water pump governor control valve, the team concluded
that for approximately
119B hours, the TDAFW pump would not have been capable
of responding
to an event. Consistent
with IMC 0609 conditional
core damage probability
assessment
methodology, this degraded condition
resulted in a loss of operability
or safety function, and therefore
was of low to moderate (B.6E-6) safety significance.
4. OTHER ACTIVITIeS
40A6 Meetings, Including
Exit On August 27 and on October 7,2009 the team presented
the inspection
results to Mr. John Carlin and other members of the R. E. Ginna Nuclear Power Plant staff. The inspectors
verified that none of the
during the inspection
is considered
proprietary
in nature. Enclosure 
A-1 ATTACHMENT
A SUPPLEMENTAL
KEY POINTS OF Licensee personnel
J. Carlin, Site Vice President
E. Larson, Plant General Manager D. Crowley, Senior Engineer E. Durkish, Associate
Engineer R. Everett, Supervisor, Primary Systems Engineering
T. Harding, Director, Licensing
R. Ruby, Principal
Engineer, Licensing
P. Swift, Engineering
Manager LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
Opened 05000244/2009008-01
Opened/Closed
05000244/2009008-02
05000244/2009008-03 Failure to Preclude Recurrence
of a Significant
Condition
Adverse to Quality Associated
with the Turbine Driven Auxiliary
Feedwater
Pump Governor Control Valve. (Section 2.1.1) Inadequate
Corrective
Actions Associated
with Steam Admission
Valve Leakage. (Section 2.1.2) Failure to Establish
Design Control Measures Associated
with the Turbine Driven Auxiliary
Feedwater
Pump Governor Control Valve. (Section 2.3) I.IST OF DOCUMENTS
REVIEWED In addition to the documents
identified
in the body of this report, the inspectors
reviewed the following
documents
and records: Corrective
Actions CA-2009-002311
Condition
Reports CR-2003-2006
CR-2005-3660
CR-2006-006029
CR-2006-006341
CR-2005-1509
CR-2005-5513
CR-2006-006204
CR-2006-006962
Attachment
CR-2007 -000876 CR-2008-009911
CR-2009-004590
CR-2009-005959*
CR-2007-001302
CR-2009-003680
CR-2009-004591
CR-2009-006765*
CR-2008-003687
CR-2009-004222*
CR-2009-005964
CR-2008-007541
CR-2009-004577
*NRC Identified
During Inspection
Corrective
Action Tracking System CATS R007325 Procedures
AP-FVV.1, Abnormal MFW Pump Flow or NPSH, Revision 01702 PT-16QT-T, Auxiliary
Feedwater
Turbine Pump -Quarterly, Revision 05900 CNG-MN-1.01-1002, Troubleshooting, Revision 0001 CNG-CA-1.01 , Corrective
Action Program, Revision 0001 CNG-CA-1.01-1004, Root Cause Analysis, Revision 0001 CNG-CA-1.01-1005, Apparent Cause Evaluation, Revision 0100 CNG-CA-1.01-1006, Common Cause Analysis, Revision 0001 CNG-CA-1.01-1007, Trending, Revision 0000 CNG-CA-1.01-1010, Use of OE, Revision 0000 IP-CAP-1, Ginna Condition
Reporting, Revision 02800 M-11.5C, Auxiliary
Feedwater
Pump Motor Mechanical
Inspection
and Maintenance, Revision 03000 0-1.1, Plant Heatup From Cold Shutdown to Hot Shutdown, Revision 16301 PT-16Q-T, Auxiliary
Feedwater
Turbine Pump -Quarterly, Revision 05600. Completed
3/14/08,514108,5/5/08,6/11/08,9/4/08, 1213/08, 1214/08, 12111/08, 12/18/08,2/12/09, 5/26/09, 5/28/09 Surveillance
Tests PT-16Q-T, Auxiliary
Feedwater
Turbine Pump -Quarterly, Revision 05600, 03/14/2008
PT-16Q-T, Auxiliary
Feedwater
Turbine Pump -. Quarterly, Revision 05700, 05/04/2008
PT-16Q-T, Auxiliary
Feedwater
Turbine Pump _. Quarterly, Revision 05700,05/05/2008
PT-16Q-T, Auxiliary
Feedwater
Turbine Pump -Quarterly, Revision 05700. 06/11/2008
STP-0-16-COMP-T, Auxiliary
Feedwater
Turbine Pump -Comprehensive Test, Revision 00000, 06/11/2008
PT-16Q-T, Auxiliary
Feedwater
Turbine Pump -Quarterly.
Revision 05701, 09/03/2008
PT-16Q-T, Auxiliary
Feedwater
Turbine Pump -Quarterly, Revision 05701, 12/02/2008
PT-16Q-T, Auxiliary
FeedwaterTurbine
Pump -Quarterly.
Revision 05701,12103/2008
PT-16Q-T.
Auxiliary
Feedwater
Turbine Pump _. Quarterly, Revision 05701, 12/04/2008
PT-16Q-T, Auxiliary
Feedwater
Turbine Pump _. Quarterly, Revision 05702, 12/11/2008
PT-16Q-T, Auxiliary
Feedwater
Turbine Pump _. Quarterly, Revision 05702, 12/18/2008
PT-16Q-T, Auxiliary
Feedwater
Turbine Pump -Quarterly, Revision 05801, 01116/2009
PT -16Q-T, AUXiliary
Feedwater
Turbine Pump -Quarterly, Revision 05801, 02112/2009
PT-16Q-T, AUXiliary
Feedwater
Turbine Pump _. Quarterly.
Revision 05900,05/26/2009
PT-16Q-T, Auxiliary
Feedwater
Turbine Pump -Quarterly, Revision 05900,05/28/2009
STP-0-16-COMP-T, Auxiliary
Feedwater
Turbine Pump -Comprehensive
Test, Revision 00400, 05/28/2009
Attachment
Work Orders W020604989
W020401907
Drawings DWG No. 33013-1231, Main Steam System, Revision 37 DWG No. 33013-2285, Motor Driven and Turbine Driven Auxiliary
Feedwater
Pumps Lube Oil Skid, Revision 17 DWG No. LB-112541, Turbine Control and Quick Start System DWG No. T040-001A, TDAFW Control Oil System, Revision 0 DWG No. T040-002A, TDAFW Turbine Trip Valve, Revision 0 DWG No. T040-003A, Auxiliary
and Standby Aux. Feedwater
Systems, Revision 2 DWG No. T040-003B, SAFW System 1-Line Diagram, Revision 0 DWG No. T040-003C, AFW System 1-Une Diagram, Revision 1 DWG No. T040-004A, Auxiliary
Feedwater
Pump Auto Start Signals, Revision 0 DWG No. T830-004A, Blowdown Isolation
Solenoid Control Circuit, Revision 0 Other Documents
Vendor Report, Preliminary
Results of Stem Sticking Failure Mechanisms, July 20, 2009 Vendor Report 09-1929 Part 1, Equipment
Root Cause Analysis of AFWP Control Valve Stem Sticking Problem at Ginna Nuclear Power Station Vendor Technical
Question Response, August 26, 2009 Category I Root Causal Analysis, May and July 2009 Turbine Driven Auxiliary
Feedwater
Pump (TDAFWP) Failures;
Overspeed
Trip During Testing vrD-E9016-4001, Excerpts from EPRI Manual 1007461, Terry Turbine Maintenance
Guide, AFW Application, Revision 000 vrD-G0153-4001, Operating
Instructions
Easy Flow Body Combined Trip Throttle Valve, Revision 2 VrD-W0315-4001, Instructions
For 465 H.P. Non-Condensing
Steam Turbine Serial Number 26635, Revision 000 VrD-W0315-4002, Service Department
Standards
Book No. 10, Field Service Manual, Revision 000 Response to NRC Generic Letter 90-3, Relaxation
of Staff Position In Generic Letter 28, Item 2.2 Part 2 "Vendor Interface
for Safety Related Components, dated September
18, 1990 CATS 10 R04451, Response to NRC IN 94-66, OVERSPEED
OF TURBINE-DRIVEN
PUMPS CAUSED BY GOVERNOR VALVE STEM BINDING CMM-37-19-9519E, Worthington
Turbine Driven Auxiliary
Feedwater
Pump Hydraulic
Governor Control Valve Maintenance
for 9519E, Revision 00200 Constellation
Energy Nuclear Generating
Group Reply to a Notice of Violation; 045 Engineering
Change Package No. ECP-2009-0146, TDAFW Lube Oil Orifice Management
Review Committee
Agenda. August 5, 2009 Purchase Requisition
No. 58686, Dresser-Rand
Valve Stem Technical
Staff Request 97-199, Leakoff from TDAFW Govenor Valve 9519E Management
Review Committee
Agenda, August 5, 2009 Purchase Requisition
No. 58686, Dresser-Rand
Valve Stem Attachment
Technical
Staff Request 97-199, Leakofffrom
TDAFW Govenor Valve 9519E Turbine Driven Auxiliary
Feedwater
Pump Preventive
Maintenance
Strategies
Auxiliary
Feed Water System, 1 st Quarter 200S Auxiliary
Feed Water System. 2nd Quarter 200S Auxiliary
Feed Water System. 3rd Quarter 200S Auxiliary
Feed Water System, 4th Quarter 200S Auxiliary
Feed Water System, 1 st Quarter 2009 Operating
Experience
OE-200S-000397
OE-200S-000607
OE-200S-000847
o E-2 0 OS-00S60 OE-2008-001296
OE-2009-00212


OE*2009*001178
J. Carlin                                      2
Oil Analysis Pump IB Oil Analysis.  
governor control valve stem and conducted weekly monitoring of the governor control valve
2008-03 Pump OB Oil Analysis, 2008-03 Reservoir
during surveillance testing to identify any potential for stem binding. In addition, corrective
Oil Analysis 2008-05 Reservoir
actions included a follow-up inspection of the governor control valve during the fall 2009
Oil Analysis 2008-08 Reservoir
  refueling outage. There is no immediate safety concern present due to this finding because the
Oil Analysis 2009-05 Attachment
system is now operable and the long term corrective actions are being implemented in Ginna's
A  
corrective action program. The final resolution of this finding will be conveyed in a separate
AV CAP CCDP CDF CR DRP EDG GEM ICCDP IMC IN INL *IPEEE LERF LOOP LOSWS NCV NRC NRR PARS PSA RCA SAFW SBO SOP SPAR SRA SCAQ NCV TBD TDAFW TS A-4 LIST OF ACRONYMS Apparent Violation
correspondence.
Corrective
As discussed in the attached Inspection report. the tinding is also an apparent violation of NRC
Action Program Conditional
requirements. specifically, 10 CFR Appendix B, Criterion XVI. "Corrective Actions." and is
Core Damage Probability
therefore being considered for escalated enforcement action in accordance with the
Core Damage Frequency
Enforcement Policy, which can be found on the NRC's Web site at http://www.nrc.gov/reading
Condition
rm/doc-collections/enforcementl.
Report Division of Reactor Projects Emergency
Following a discussion of the preliminary safety Significance of this finding during the initial exit
Diesel Generator
briefing on August 27,2009. a phone call was held between Glenn Dentel, Branch Chief,
Graphical
Division of Reactor Projects. and yourself on October 1. 2009. During this call, you indicated
Evaluation
that R.E. Ginna Nuclear Power Plant does not contest the characterization of the rIsk
Module Incremental
significance of this finding, and therefore you have declined to further discuss this issue at a
Conditional
Regulatory Conference or provide a written response. Please note that by declining to request
Core Damage Probability
a Regulatory Conference or submit a written response, you relinquished your right to appeal the
Inspection
final SOP determination. in that by not doing either, you would not meet the appeal
Manual Chapter Information
requirements stated in the Prerequisite and Limitation sections of Attachment 2 of IMC 0609.
Notice Idaho National Labs Individual
You will be advised by a separate correspondence of the results of our deliberations on this
Plant Examination
matter.
of External Events Large Early Release Frequency
In addition. the report documents two findings of very low safety significance (Green). The
Loss of Off site Power Loss of Service Water System Non Cited Violation
findings involved violations of NRC requirements. However, because of the very low safety
Nuclear Regulatory  
significance and because they are entered into your corrective action program (CAP). the NRC
Commission
is treating these findings as non-cited violations (NeVs) consistent with Section VI.A.1 of the
Office of Nuclear Reactor Regulation
NRC Enforcement Policy. If you contest any NCV in this report, you should provide a response
Publicly Available
within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear
Records Probabilistic
Regulatory Commission, A TIN.: Document Control Desk, Washington, DC 20555-0001; with
Safety Assessment
copies to the Regional Administrator, Region I; the Director, Office of Enforcement; and the
Root Cause Analysis Standby Auxiliary
NRC Resident Inspector at R.E. Ginna. In addition. if you disagree with the characterization of
Feedwater
any finding in this report, you should provide a response within 30 days of the date of this
Station Blackout Significance
inspection report. with the basis for your disagreement, to the Regional Administrator, Region I,
Determination
and the NRC Resident Inspector at R.E. Ginna Nuclear Power Plant. The information you
Process Standardized
provide will be considered in accordance with Inspection Manual Chapter 030?
Plant Analysis Risk Senior Reactor Analyst Significant
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its
Condition
enclosure, and your response (if any) will be available electronically for public inspection in the
Adverse to Quality Non-citied
 
Violation
J. Carlin                                  3
To Be Determined
NRC Public Document Room or from the Publicly Available Records (PARS) component of the
Turbine Driven Auxiliary
NRC's document system (ADAMS). ADAMS is accessible from the NRC Web Site at
Feedwater
http://www.nrc.gov/reading-rm/adams.html(the Public Electronic Reading Room).
Technical
                                          Sincerely,
Specification
                                                ,/;I,/;tJ
Attachment
                                          D~ew,~~ --fbr-
                                          Division of Reactor Projects
8-1 Special Inspection R.E. Ginna Nuclear Power Failure of the Turbine-Driven
Docket No.: 50-244
Auxiliary
License No.: DPR-18
Feedwater (TDAFW) on May 26, 2009 and July 2, Background:
Enclosures:    Inspection Report 05000244/2009008
On May 26, 2009, during routine
              w/Attachment A: Supplemental Information
quarterly
              w/Attachment B: Special Inspection Charter
surveillance
cc w/encl: Distribution via ListServ
testing of the turbine driven auxiliary
 
feedwater (TDAFW) system, the TDAFW pump tripped on overspeed.  
J. Carlin                                                  2
The test was repeated several hours later and the TDAFW pump tripped again on overspeed.
NRC Public Document Room or from the Publicly Available Records (PARS) component of the
Fluctuations
NRC's document system (ADAMS). ADAMS is accessible from the NRC Web Site at
in oil pressure were observed during the testing. After extensive
httg:llwww.nrc.gov/reading*rm/adams.html(the Public Electronic Reading Room).
troubleshooting, Ginna
                                                          Sincerely,
identified
                                                          IRAJ James W. Clifford for:
a number of issues but no definitive
                                                          David C. lew, Director
cause for the overspeed
                                                          Division of Reactor Projects
trips. The lube/control
Docket No.: 50-244
oil system was drained and cleaned due to the presence of fine particulates;
License No.: DPR-18
a pressure pulsation
Enclosures:          Inspection Report 05000244/2009008
dampener accumulator
                    w/Attachment A: Supplemental Information
bladder was replaced due to a below normal pressure condition;
                    w/Attachment B: Special Inspection Charter
the oil pressure regulating
cc w/encl: Distribution via ListServ
bypass valve was replaced due to potential
SUNSI Review Complete:                    gtd                (Reviewer's Initials)
cycling; a change to linkage setup was implemented;  
DOCUMENT NAME: G:\DRP\BRANCH1\Ginna\TDAFW SIT\AED Track Changes Ginna SIT
governor relay valve, and trip and throttle valve parts were replaced due to out of specification
Report Rev 4 cC.doc
clearances;
After declaring this document "An Official Agency Record" it will be released to the Public.
and a miSSing oil line orifice was installed.  
To receive I!I copy of this document, indicate in the box: "C' =Copy without attachmenVenclosure "e" = Copy with
Following
attaclhmentlenclosure "N";:; No co                                                                      ML093160122
these corrective
OFFICE            RI/DRS                                                RI/ENF                  RI/DRP
actions, the system was successfully
NAME              CCahill/cc*                                                                  JClifford/jwc
tested and declared operable.  
DATE              10/21109                                                                      11/05/09
Constellation
                              *see prior concurrence OFFICIAL RECORD COpy
is completing
Distribution w/encl:
a root cause evaluation
S. Collins, RA (R10RAMaii Resource)                                ROPreports@nrc.gov
and the resident inspectors
M. Dapas, ORA (R10RAMaii Resource)
continue to conduct baseline inspections
D. Lew, DRP (R1DRPMaii Resource)
with assistance
J. Clifford, DRP (R1DRPMail Resource)
from DRS specialists.  
l. Trocine, RI OEDO
Testing of the TDAFW system will be at an increased
RidsNrrPMREGinnaResource
frequency
RidsNrrDorlLpl1-1 Resource
until Constellation
G. Dentel, DRP
has confidence
N. Perry, DRP
that the system is performing
J. Hawkins, DRP
as required.
K. Kolaczyk, DRP, SRI
On July 2, 2009, during the performance
S. Kennedy, DRP, SRI
of the increased
L. Casey, DRP, RI
frequency
M. Rose, DRP, OA
surveillance, the TDAFW pump again tripped on overspeed.  
D. Bearde, DRP
Glnna personnel
 
discovered
                                      1
pitting and corrosion
                U.S. NUCLEAR REGULATORY COMMISSION
on the stem of the governor control valve during troubleshooting
                                  REGION I
activities
Docket No.: 50-244
to restore the pump to operable status. This Special Inspection
License No.: DPR-18
Team had raised concerns regarding
Report No.:  05000244/2009008
corrosion
Licensee:    Constellation Energy, R. E. Ginna Nuclear Power Plant, LLC
on the stem of the Governor Control Valve during onsite inspection
Facility:    R. E. Ginna Nuclear Power Plant
activities
Location:    Ontario. New York
the week of June 15, 2009. Basis for the Formation
Dates:      June 15-19, 2009 and August 24-27.2009
of the SIT: The failure of the TDAFW pump involved repetitive
Team Leader: C. cahill, Senior Reactor Analyst, Division of Reactor Safety
failures of this
Inspectors:  S. Kennedy, Senior Resident Inspector, Division of Reactor Projects
eqUipment.  
            K. Kolaczyk, Senior Resident Inspector, Division of Reactor Projects
There have been three failures of the TDAFW pump since December 2008. On December 2, 2008, a failure was attributed
            J. Bream, Project Engineer. Division of Reactor Projects
to inadequate
Approved by: Glenn T. Dentel, Chief
implementation
            Projects Branch 1
of the preventive
            Division of Reactor Projects
maintenance
 
program. SpeCifically, the governor linkages were not lubricated
                                                    2
in March 2008 which resulted in the pump's inability
                                      SUMMARY OF FINDINGS
to achieve the required flow and pressure in December 2008. On July 2, 2009, the failure was preliminarily
IR 05000244/2009008; 06/15-19/2009 and 08/24-2'712009; R. E. Ginna Nuclear Plant; Special
determined
Inspection Team Report.
to be caused by pitting on the stem of the Governor Control valve and overly tolerances
The report covered two on-site inspection visits and related in-office inspection activities by a
causing binding of the stem. Although the specific failure modes (overspeed
special inspection team consisting of a Senior Reactor Analyst. two Senior Resident Inspectors.
trip, inability
and one Project Engineer. One apparent violation (AV) with potential for greater than Green
to achieve the required flow or pressure)
safety significance and two Green findings were identified. The significance of most findings is
were different, the underlying
indicated by its color (Green. White, Yellow, or Red) using Inspection Manual Chapter (lMC)
cause of inadequate
0609, "Significance Determination Process." Findings for which the significance determination
or inappropriate
(SDP) process does not apply may be Green or be assigned a severity level after NRC
preventive
management review. The NRC program for overseeing the safe operation of commercial
maintenance
nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 4,
may be the same. Attachment
dated December 2006.
8  
NRC Identified and Self-Revealing Findings
Based upon best available
Cornerstones: Mitigating Systems
information, the Region I Senior Reactor Analyst (SRA) conducted
        Preliminary White: A self-revealing apparent violation (AV) of 10 CFR 50, Appendix B,
a preliminary
        Criterion XVI, uCorrective Actions," was identified for the failure to preclude recurrence
risk estimate of the May 26 TDAFW pump failure. An incremental
        of a signIficant condition adverse to quality (SCAQ) associated with the Turbine Driven
conditional
        Auxiliary Feedwater (TDAFW) pump governor control valve. Specifically, after
core damage probability (ICCDP) in the upper E-6 range (8E-6 per the 82 day exposure period), was calculated
        identifying corrosion of the govemor control valve stem in April 2005, Ginna did not take
using the Ginna SPAR model. assuming that the TDAFW pump would not have started since the last time it passed a surveillance
        adequate corrective actions to preclude the recurrence of corrosion which led to the
test on March 5 until May 26 (82 days). The dominant core damage sequence was a station blackout (LOOP with failure of both EDGs,) with no TDAFW and failure to recover offsite power or an EDG in one hour. Based upon the preliminary
        binding of the gavemar control valve and failure of the TDAFW pump on July 2,2009.
conditional
        In addition, the inspectors concluded that governor control valve stem binding was the
core damage probability
        likely cause of the failure of the TDAFW pump on May 26,2009. The overspeed trip of
estimate of upper E-6 range, in accordance
        the TDAFW pump on May 26. 2009. was originally determined by Ginna to be failure of
with IMC 0309, this event falls within the region for a Special Inspection
        the governor control system relay valve. Governor control valve stem corrosion is a
Team. Oblectives
        SCAQ because corrosion of the stem can IHad to governor control valve stem binding
of the Special Inspection:
        and failure of the TDAFW pump as discussed in NRC Information Notice (IN) 94-66:
The objectives
        "Overspeed of Turbine-Driven Pumps Caused by Governor Valve Stem Binding" and
of the special inspection
        other related industry operating experience documents. Immediate corrective actions
are to review and assess: (1)
        inCluded entering this condition in the corrective action program (CAP). conducting a
Constellation's
        root cause analysis (RCA). replacing the governor control valve stem, and conducting
planning and execution
        weekly monitoring of the governor control valve during surveillance testing to identify
of the risk significant
        any potential for stem binding. In addition, corrective actions included a follow-up
work activities
        inspection of the governor control valve during the fall 2009 refueling outage. Ginna will
on the TDAFW system; (2) equipment
        continue to monitor the govemor control valve under an enhanced TDAFW surveillance
issues related to the TDAFW testing; and (3) Constellation's
        program to ensure TDAFW pump operability.
response to this significant
        The finding is more than minor because it is associated with the equipment performance
equipment
        attribute of the Mitigating System cornerstone and affects the cornerstone objective to
failure. To accomplish
        ensure the availability, reliability, and capability of systems that respond to initiating
these objectives, the following
        events to prevent undesirable consequences. Specifically. stem corrosion caused
will be performed: Evaluate the adequacy and completeness
        binding of the governor control valve and led to the failure of the TDAFW pump. This
of the maintenance
        finding was assessed using IMC 0609 and preliminarily determined to be White (lOW to
on the TDAFW system, including
        moderate safety significance) based on a Phase 3 analysis with a total (internal and
preventive
                                                                                            Enclosure
maintenance, procedural
 
guidance, maintenance
                                              3
testing, and supervisory
external contributions) calculated conditional core damage frequency (CCDF) of B.6E-6.
oversight. Evaluate Constellation's
This finding has a cross-cutting aspect in the area of Problem Identification and
application
  Resolution, Corrective Action Program, because Ginna did not implement a corrective
of pertinent
  action program with a low threshold for identifying issues completely, accurately, and in
industry operating
  a timely manner commensurate with their safety significance [P.1(a} per IMC 0305].
experience
Specifically, Ginna did not identify issues a~;sociated with corrosion of the governor
and evaluation
control valve within the corrective action program. (Section 2.1.1)
of potential
Green: A self-revealing non-cited violation (NCV) of 10 CFR 50, Appendix B, Criterion
precursors, including
XVI, "Corrective Actions," was identified for the failure to establish adequate measures
the effectiveness
to correct a longstanding issue associated with steam admission valves leakage. As a
of any actions taken in response to the operating
  result, the leakage most likely contributed to the build-up of corrosion on the TDAFW
experience
pump governor control valve stem and contributed to the failure of the TDAFW pump on
or precursors. Evaluate the adequacy of Constellation's
May 26, 2009, and on July 2, 2009. The steam admission valves had been leaking
response to the TDAFW system failures, including
since at least 2005. However, G.inna did not take adequate measures to correct the
Constellation's
leakage or minimize the impact of the leakage on governor control valve performance.
cause analysis and completed
Immediate corrective actions included entering this condition in the corrective action
interim corrective  
program, conducting a root cause analysis, replacing the governor control valve stem,
actions. Evaluate the adequacy of Constellation's
and conducting weekly monitoring of the governor control valve during surveillance
initial extent of condition
testing to identify any potential for stem binding. Additionally, the steam admission
for the TDAFW failures, as appropriate. Evaluate the failure modes for potential
valves were inspected and re-worked and the governor control valve was inspected
generic implications
during the fall 2009 outage. Ginna will continue to monitor the governor control valve
including
under an enhanced TDAFW surveillance program to ensure TDAFW pump operability.
the need for generic communications
Planned corrective actions include replacin~~ the steam admission valves in May 2011.
Additionally, the team leader will review lessons learned from the Special Inspection
The finding is more than minor because it is associated with the equipment performance
and, if appropriate, prepare a feedback form on recommendations
attribute of the Mitigating Systems cornerstone and affects the cornerstone objective to
for revising the reactor oversight
ensure the availability and reliability of systems that respond to initiating events to
process (ROP) baseline inspection
prevent undesirable consequences. Specifically, leakage through the steam admission
procedures
valves can result in continuous wetting of the governor control valve stem and lead to or
in order to proactively
accelerate corrosion of the governor control valve. This could result in a stem binding of
identify the issues and causes involved with the event. Guidance:
the governor control valve and failure of the TDAFW pump. The inspectors evaluated
Inspection
the signifiCance of this finding using IMC 0609, Attachment 4, "'Phase 1 - Initial
Procedure
Screening and Characterization of Findings." The finding is of very low safety
93812, "Special Inspection", provides additional
significance because it is not a design or qualification deficiency, did not represent a
guidance to be used by the Special Inspection
loss of a safety function of a system or a single train greater than its technical
Team. Team duties will be as described
speCification (TS) allowed outage time, and did not screen as potentially risk Significant
in Inspection
due to external events. This finding has a cross-cutting aspect in the area of Problem
Procedure
Identification and Resolution, Corrective Action Program, because Ginna did not
93812. The inspection
thoroughly evaluate problems such that the resolutions address causes and extent of
should emphasize
conditions, as necessary, In a timely manner, commensurate with their significance
fact-finding
[P.1 (c) per IMC 0305]. Specifically, Ginna did not thoroughly evaluate the potential
in its review of the circumstances
effect of the steam admission valve leakage on the governor control valve performance.
surrounding
(Section 2.1.2)
the event. It is not the responsibility
Green: The inspectors identified an NCVof 10 CFR 50, Appendix B. Criterion III,
of the team to examine Attachment
"Design Control," for the failure to establish measures to ensure that a modification
performed on the governor control valve bushing was a suitable application of materials
the regulatory
for the TDAFW pump. During a review of the RCA associated with the TDAFW pump
process. Safety concerns identified
failures, the inspectors noted that Ginna did not consider the potential impact of
that are not directly related to the event should be reported to the Region I office for appropriate
                                                                                    Enclosure
action. The Team will conduct an entrance meeting and begin the inspection
 
on June 8,2009. While on site, the Team Leader wi" provide daily briefings
                                                    4
to Region I management, who will coordinate
      removing some of the hardened layer of the bushing on the corrosion rate of the
with the Office of Nuclear Reactor Regulation, to ensure that all other parties are kept informed.
      governor control valve. Following concerns raised by the inspectors, Ginna inspected
A report documenting
      the governor control valve bushing during the fall 2009 refueling outage and observed
the results of the inspection
      corrosion of the bushings. Ginna noted that the corrosion of the bushings appeared to
should be issued within 45 days of the completion
      have been caused by the lapping of the bushing to achieve the increased clearance
of the inspection.  
      between the stem and the bushings. Immediate corrective actions following the
This Charter may be modified should the team develop significant
      inspection of the governor control valve during the fall 2009 refueling outage included
new information
      entering this condition in the CAP and refurbishing the governor control valve with a new
that warrants review. Attachment  
      stem and bushing.
8
      The finding is more than minor because it is associated with the equipment performance
      attribute of the Mitigating System cornerstone and affects the cornerstone objective to
      ensure the availability, reliability, and capability of systems that respond to initiating
      events to prevent undesirable consequences. Specifically, lapping of the valve bushing
      resulted in an unanticipated corrosion mechanism of the govemor control valve that
      impacted the reliability of the TDAFW pump" The inspectors evaluated the significance
      of this finding using IMC 0609, Attachment 4. "Phase 1 Initial Screening and
      Characterization of Findings." The finding is of very low safety significance because it is
      a design or qualification deficiency confirmed not to result in the loss of operability or
      functionality. The inspectors determined that this finding has a cross-cutting aspect in
      the area of Human Performance, Decision Making. because Ginna did not make a
      safety-significant or risk-significant decision using a systematic process, especially when
      faced with uncertain or unexpected plant conditions, to ensure safety was maintained
      [H.1(a) per IMC 0305]. Specifically, Ginna did not use a systematic process such as an
      engineering evaluation to properly evaluate the potential impact of removing some of the
      hardened layer of the bushing. [H.1 (a) per IMC 0305]
      (Section 2.3)
Licensee Identified Violations
      None
                                                                                          Enclosure
 
                                                5
                                      REPORT DETAILS
1.  INTRODUCTION
1.1  Background and Event Description
    On May 26, 2009, and July 2, 2009, the TDAFW pump tripped on overspeed during the
    performance of surveillance testing activities. These were the second and third times
    the TDAFW pump had failed a surveillance test in a six month period. The previous test
    failure occurred on December 2, 2008, when the TDAFW pump failed to develop
    acceptable discharge pressure during a quarterly surveillance test. Details surrounding
    the December test failure including Ginna corrective actions are discussed in NRC
    Integrated Inspection Report 50-244/2009002. Following each of the three test failures,
    Ginna declared the TDAFW pump inoperable and entered the limiting Condition for
    Operation for TS 3.7.5 "Auxiliary Feedwater."
    Following the May 26, 2009, test failure, Ginna troubleshooting activities were focused
    on the TDAFW lubricating oil system where system pressure oscillations were noted by
    test personnel prior to the pump overspeed trip. As part of the troubleshooting efforts,
    the TDAFW lubricating oil system was drained and refilled with fresh oil, filters in the
    lubrication system were examined and replaced, and several components in the
    lubricating oil system including the relay and pressure regulating valves were replaced.
    Additionally the turbine governor linkage was adjusted to original specifications outlined
    in the vendor technical documents. Although several out of speCification and missing
    components were identified during this troubleshooting effort, a definitive cause for the
    surveillance failure was not identified. Nevertheless, following the successful completion
    of post maintenance testing activities, Ginna declared the TDAFW pump operable and
    commenced an augmented surveillance testing program for the TDAFW pump that
    tested the pump on a weekly basis.
    On July 2, 2009, another TDAFW pump overspeed failure occurred when the pump was
    undergoing the augmented testing program. Troubleshooting activities following this
    failure were focused on the turbine control system, which did not appear to have
    functioned properly during the test. Accordingly, the turbine control and relay valves
    were disassembled and inspected, and the governor linkage system was adjusted.
    Additionally. the lubricating oil system was flushed and examined for particulates.
    However, unlike the May 26 failure, these troubleshooting activities identified a definitive
    cause, a stuck governor control valve stem, that resulted in the surveillance test failure.
    Visual inspection of the stem, which had become bound to its bushing and had to be
    forcibly removed, revealed corrosion buildup where the stem contacted the upper valve
    bushing. To restore the control valve to an operable status, Ginna replaced the valve
    stem and increased the bushing clearances to dimensions specified by the Ginna
    TDAFW pump inspection procedure. The pump was successfully tested and declared
    operable subject to an augmented testing program.
    Ginna assigned an RCA team to investigate the surveillance test failures. The Ginna
    RCA team concluded that the primary root cause of the failure of the governor contrOl
    valve to control turbine speed on July 2,2009, was binding caused by a corrosion
    mechanism that occurred between the valve stem and the valve bushings. The RCA
    team also concluded that stem binding appeared to be an intermittent problem and that
                                                                                      Enclosure
 
                                                6
      station members missed opportunities to identify the failure mode during previous
      surveillances and failures. As such, the RCA team determined that governor control
      valve stem binding could not be ruled out as a possible failure mode during the
      December 2008 and the May 2009 TDAFW pump failures.
    At Ginna's request, an independent vendor reviewed the issues associated with the
      governor control valve stem binding to determine the failure mechanism that was the
      cause of the TDAFW pump overspeed trips. The vendor determined that the most likely
      cause of the corrosion of the governor control valve stem was fresh-water corrosion
    (Langelier corrosion) that was the result of galvanic interactions between the nitrided
    case and the base material of the governor control valve stem. The vendor considered
    several variables that contributed to the corrosion mechanism such as material
      composition of the stem and bushing, stem-to-bushing clearance, steam admission
    valve leakage, and TDAFW pump surveillance frequency and duration.
1.2 Special Inspection Scope
    The NRC conducted this inspection to gain a better understanding of the circumstances
    involving the TDAFW pump overspeed trips during surveillance testing on May 26, 2009,
    and on July 2,2009. The inspection team used NRC Inspection Procedure 93812,
    "Special Inspection," as a guide to complete their review. Additional inspection and
    review activities were outlined in the special inspection team charter, provided as
    Attachment B. The special inspection team reviewed procedures, corrective action
    documents, work orders, engineering analyses, and the root cause evaluation prepared
    by Ginna. In addition. the team conducted equipment walkdowns and interviewed key
    plant personnel regarding the discovery and resolution of the condition. A list of site
    personnel interviewed and documents reviewed are provided in Attachment A to this
    report.
1.3  Preliminary Conditional Risk Assessment
    Using IMC 0309, "Reactive Inspection Decision Basis for Reactors," IMe 0609,
    "Significance Determination Process," and the Ginna Standardized Plant Analysis Risk
    (SPAR) model in conjunction with the Graphical Evaluation Module (GEM). the Region I
    Senior Reactor Analyst (SRA) evaluated the increase in conditional core damage
    probability for the failure of the TDAFW pump. Based on the nature of the failure and
    the subsequent overspeed trip on an instrumented diagnostic run, the condition was
    evaluated as being non-recoverable in the event of actual demand.
      Based upon best available information, an incremental conditional core damage
      probability (ICCDP) in the upper E-6 range (8E-6 per the 82 day exposure period), was
      calculated. The exposure period was based on the assumption that the TDAFW pump
      would not have started since the last time it passed a surveillance test on March 5 until
      May 26 (82 days). The dominant core damage sequence was a station blackout (loss of
      offsite power (LOOP) with failure of both emergency diesel generators (EDGs), with no
      TOAFW and failure to recover offsite power or an EDG in one hour.
    Based upon this conservative conditional core damage probability (CCDP) value, and
    having satisfied an IMC 0309 deterministic criterion, the May 26 degraded TDAFW pump
                                                                                      Enclosure
 
                                                  7
      condition fell within the Special Inspection to Augmented Inspection Team range for
      reactive inspections.
2.    SPECIAL INSPECl"ION AREAS
2.1    Review of Maintenance
a.    Inspection Scope
      The team evaluated the adequacy and completeness of the maintenance on the TDAFW
      system, including preventive maintenance, procedural guidance, post-maintenance
      testing, and supervisory oversight. The team independently evaluated selected
      procedures, preventive maintenance strategies. condition reports (CRs). system health
      reports. and associated work orders. In addition, the team reviewed the RCA,
      conducted equipment walkdowns and interviewed key station personnel. For the
      weaknesses identified, the inspectors verified that appropriate corrective actions have
      been planned or taken.
b.    Findings and Observations
  1.  Failure to Preclude Recurrence of a Significant Condition Adverse to Quality
      Introduction: A self-revealing AV of 10 CFR 50, Appendix S, Criterion XVI, "Corrective
      Actions," was identified for the failure to preclude recurrence of a SCAQ associated with
      the TDAFW pump governor control valve. Specifically, after identifying corrosion of the
      governor control valve stem in April 2005, Ginna did not take adequate corrective
      actions to preclude the recurrence of corrosion which led to the binding of the governor
      control valve and failure of the TDAFW pump on July 2, 2009. In addition, governor
      control valve stem binding was a fikely failure of the May 26, 2009, TDAFW pump
      overspeed trip. This finding was preliminarily determined to be White.
      Description: On April 11, 2005, Glnna conducted a periodic major inspection of the
      TDAFW pump governor control valve under work order #20401907. During the
      disassembly of the valve, mechanics noted corrosion in the bushing area of the stem
      plug. The vendor recommended replacing the valve stem and plug due to the corrosion.
      However, Ginna did not recognize stem corrosion as a condition adverse to quality and
      did not initiate a CR in accordance with station guidance in IP-CAP-1 r "Condition
      Reporting." As a result, Ginna did not conduct any further analysis or evaluation to
      determine the cause of the corrosion. On July 2, 2009, during surveillance testing, the
      TDAFW pump tripped due to overspeed. Ginna formed an Issue Response Team and
      developed a comprehensive troubleshooting plan to determine the cause(s) of the
      failure. The troubleshooting plan consisted of all possible failure modes, possible
      causes of each failure mode, and actions to validate or refute each "failure mode. Upon
      disassembly of the governor control valve, the stem was found seized within its bushings
      and had to be forcibly removed. Visual inspection showed pitting on the surface of the
      stem Where it contacted the upper valve bushing. Following completion of the
      troubleshooting activities, Ginnaconcluded that TDAFW pump failure was due to binding
      of the governor control valve and that the binding was caused by the build up of
      corrosion on the valve stem.
                                                                                      Enclosure
 
                                              8
  Governor control valve stem corrosion is an SCAQ because corrosion of the stem can
  lead to govemor control valve stem binding and failure of the TDAFW pump as
  discussed in NRC IN 94-66: "Overspeed of Turbine-Driven Pumps caused by Governor
  Valve Stem Binding," and other related industry operating experience documents.
  Immediate corrective actions included entering this condition in the CAP, conducting an
  RCA, replacing the governor control valve stem, and conducting weekly monitoring of
  the governor control valve during surveillance testing to identify any potential for stem
  binding. In addition, corrective actions included a follow-up inspection of the governor
  control valve during the fall 2009 refueling outage. Because additional corrosion was
  found during this inspection on September 18, 2009, the control valve was sent to the
  vendor to be refurbished. Ginna will continue to monitor the governor control valve
  under an enhanced TDAFW surveillance program to ensure TDAFW pump operability.
  Ginna also was evaluating longer term corrective actions to address the corrosion
  including more frequent governor control valve stem replacement, change of the stem
  material, and other modifications to the system design. Planned corrective actions
  include replacing the stem admission valves in May 2011.
  The inspectors noted that governor control valve stem binding also could have been a
  contributor to the December 2, 2008, TDAFW pump failure to develop the minimum
  acceptable discharge flow and pressure, and the likely cause of the May 26, 2009,
  TDAFW pump overspeed trip. Following these events, Ginna missed opportunities to
  identify potential stem binding problems after identifying possible indicators of this failure
  mode such as leaking steam admission valves and rust/corrosion on the visible portion
  of the governor valve stem. In addition, during troubleshooting efforts in May 2009,
. Ginna missed an opportunity to exercise the governor control valve stem with the linkage
  disconnected and lube oil pressure not applied. Operating experience suggested that
  cycling the valve by hand without hydraulics applied is a prudent action to validate or
  refute governor control valve stem binding.
  Analysis: The performance deficiency is that Ginna did not take adequate measures to
  correct a condition that had the potential to impact the operability of the TDAFW pump.
  Specifically, after identifying corrosion on the governor control valve stem in 2005, Ginna
  did not take adequate corrective actions to preclude the recurrence of corrosion which
  led to the binding of the governor control valve and failure of the TDAFW pump. The
  finding is more than minor because it is associated with the equipment performance
  attribute of the Mitigating System cornerstone and affects the cornerstone objective to
  ensure the availability, reliability, and capability of systems that respond to initiating
  events to prevent undesirable consequences. Specifically, stem corrosion caused
  binding of the governor control valve and led to the failure of the TDAFW pump.
  In accordance with IMe 0609, Attachment 4, "Phase 1 - Initial Screening and
Characterization of Findings," a Phase 2 risk analysis was required because the finding
represents an actual loss of safety function of a single train for greater than the TS
allowed outage time of 7 days. The Phase 2 risk evaluation was performed in
accordance with IMC 0609, Appendix A, Attachment 1, "User Guidance for Phase 2 and
Phase 3 Reactor Inspection Findings for At*,power Situations." Because the precise time
is unknown for the inception of TDAFW pump inoperability, an exposure time of one-half
of the time period (t/2) between discovery (May 26, 2009) to the last successfully
completed quarterly surveHlance test (March 5, 2009) was used. This t/2 exposure time
                                                                                      Enclosure
 
                                              9
equals 51 days. Using Ginna's Phase 2 SDP notebook, pre-solved worksheets, and an
initiating event likelihood of 1 year (>30-days exposure time), the inspector identified that
this finding is of potentially substantial safety significance (Yellow). The dominant
sequence identified in the Phase 2 notebook involves a loss of offsite power (LOOP),
failure of both EDGs, and the subsequent loss of the TDAFW pump, with the failure of
operators to restore offsite power within 1 hour: LOOP (2) + EAC (3) + TDAFW (0) +
REC1 (0) = 5 (Yellow). In recognition that the Phase 2 notebook typically yields a
conservative result, a NRC Region I Senior Reactor Analyst (SRA) performed a Phase 3
risk assessment of this finding.
The SRA used Ginna's Standardized Plant Analysis Risk (SPAR) model, Revision 3.45,
dated June 2008. and graphical evaluation module, in conjunction with the System
Analysis Programs for Hands-On Integrated Reliability Evaluations (SAPHIRE). Version
7, to estimate the internal risk contribution of the Phase 3 risk assessment. The
following assumptions were used for this assessment:
    1. Based on the guidance provided in the Risk Assessment of Operational Events
          Handbook, Revision 1.01, the calculated exposure was determined to be 1198
          hrs. The summation of this exposeure time was determined as follows:
              * One half the exposure time, (tI2), was applied for the period between
                  March 5 - May 26, 2009
              * The full exposure time, (t). was applied for the unavailability and
                  troubleshooting from May 26 - May 29, 2009.
              * One half the exposure time. (tI2), was applied for the period between
                  June 25 -July 2, 2009
              * The full exposure time, (t), was applied for the unavailability and
                  troubleshooting from July 2 - July 5, 2009
    2. To closely approximate the type of flilure exhibited by the TDAFW pump, the fail
        to start basic event <AFW-TDP-FS-TDP> was changed from its baseline failure
        probability to 1.0, representing a 100 percent failure to start condition.
    3. Based on the nature of the failure. and no recovery procedures in place, there
        was no recovery credit assigned to the May failure.
    4. The loss of service water initiating event frequency (IE-LOSWS) was increased
        from its nominal value of 4.0E-4 to 2.0E*3 to more closely model the risk of a
        LOSWS at the Ginna station. This is consistent with Ginna's understanding of
        the risk of this event. All remaining events were left at their nominal failure
        probabilities.
    5, The model was modified by Idaho National Laboratory (INL) to include
        convolution correction factors. Convolving the failure distribution eliminates the
        simplifying assumption that all failure to run events happen at time=O. Inclusion
        of this correction can reduce station blackout (SBO) core damage frequency
        (CDF) significantly for plants like Ginna that have low EDG redundancy.
    6. Since all observed failures happened upon the initiation of the TDAFW system,
        the period between May 29 and June 25 2009, was not included in the exposure
        period because the system successfully completed increased, weekly,
        surveillance testing. The team could not conclude that the stem binding
        condition would occur after the pump had been successfully started and run.
    7. Cutset probability calculation truncation was set at 1E-13.
                                                                                    Enclosure
 
                                              10
  Based upon the above assumptions, the Ginna SPAR model calculated an increase in
  internal event contribution to conditional core damage probability (CCDP) of 2.9E-6. This
  low-ta-mid E-6 delta CCDP value represents a low to moderate safety significance
  (White). The dominant internal event sequence involved a LOOP with subsequent
failure of the EDGs (station blackout event), the failure of the TDAFW train and the
failure to recover AC power. The Phase 3 SPAR model results correlate well to the
  Phase 2 SDP Notebook dominant core damage sequences.
  External Events Risk Contribution
The Ginna Probablistic Safety Assessment (PSA) includes a Level 1 analysis of fires
and flooding external events. The PSA summarizes the fire contribution as representing
approximately 48% of the total (internal and external) core damage frequency, or nearly
half of the annualized risk. The NRC does not have an external event risk model for
Ginna. Consequently, the SRA, after review of the licensee's Individual Plant
Examination of External Events (IPEEE), utilized the licensee's external events
assessment to quantify the fire and flooding events risk contribution for this condition.
Seismic event likelihood was considered to be very low and determined not to be a
significant contributor to the risk of this condition.
The results of the PSA for this condition calculated a CCDP contribution from fire events
at 5E-6 and from flooding at 7E-7. The most significant fire initiated core damage
sequence involved a spectrum of control room fires, with a failure of automatic and
manual suppression, a failure of the TDAFW pump and a failure of the 'C' standby
auxiliary feed water pump for decay heat removal via the steam generators. The most
Significant flooding core damage sequence quantified in the PSA for this condition,
Involved flooding in the relay room, failure of the TDAFW pump and a failure to align
standby auxiliary feed water pump for decay heat removal via the steam generators.
Large Early Release Frequency (LERF) Evaluation
The SRA used IMC 0609, Appendix H, "Containment Integrity Significance
Determination Process," to determine if this finding was a significant contributor to a
large early release. The Ginna containment is classified as a pressurized water reactor
large-dry containment deSign. Based upon the dominant sequences involving LOOP
and station blackout (S80) initiating events, per Appendix H, Table 5.2, "Phase 2
Assessment Factors - Type A Findings at Full Power," the failure of the TDAFW pump
does not represent a significant challenge to containment integrity early in the postUlated
core damage sequences. Consequently, this finding does not screen as a significant
large early release contributor because the close-in populations can be effectively
evacuated far in advance of any postulated release due to core damage, Accordingly,
the risk significance of this finding is associated with the delta CDF value, per IMC 0609,
Appendix H, Figure 5.1, and not delta LERF.
Risk Assessment Summary
The calculated total risk significance of this finding is based upon the summation of
internal and external risk contributions (delta CCDP internal + delta CCDP external (fires
and floods).= delta CCDP total). 2.9E-6 + 5E-6 + 7E-7 = 8.6E-6 delta ceDP.
                                                                                  Enclosure
 
                                                11
Annualized, this value of 8.6E-6 delta CDF represents a low to moderate safety
significance or White finding.
Licensee's Risk Assessment Summary
Constellation's risk assessment for the given condition, assuming no operator recovery,
resulted in a total delta CDF value of 1.028E-5. This increase in CDF value comprised
of: 4.6E-6 due to intemal events; 0.7E-6 due to intemal flooding events; and 5E-6
fire/external events. Similar to the NRC internal risk contribution, the largest percentage
of intemal risk was derived from station blackout events. The licensee conducted
refinements in their modeling to credit additional recovery options in the event that the
TDAFW pump failed. By crediting these recovery actions, the delta CDF was reduced
from 1.028E-5 to 9.2 E-6, or by approximately 10%. The specific recovery actions are
as follows:                                    .
    1. The potential for operators to use standby auxiliary feedwater (SAFW) pump C,
          in lieu of the TDAFW pump during fire and flood scenarios which require use of
          alternate shutdown procedures was modeled. Although use of an SAFW pump
          is not specifically called out in these procedures, the procedures do explicitly
          recognize that if the TDAFW pump is not functioning, a loss of secondary heat
          sink will result, and direct operators to refer to other emergency procedures for
        alternate methods of establishing a heat sink (see ER-FIRE.1 step 4.3.4.2, ER
          FIRE.2 step 4.3.12, etc.}. In response to this hypothetical scenario, an
        operations Shift Manager (SM) indicated that upon a failure of the TDAFW to
          provide flow, a SAFW pump could be manually started by locally opening the
        service water suction valve to the pump and locally closing the breaker to the
        pump motor. The steps necessary to align an SAFW pump to the steam
        generators (SG) are contained in emergency operating procedures (EOP)
        Attachment 5.1 'Attachment SAFW'. Since only Busses 14 and 18 are energized
        during ER-FIRE scenarios, SAFW pump C would be used.
    2. Following the May 26th overspeed trip of the TDAFW pump, new section 2.2
        was added to procedure P-15.6, 'Operation of the TDAFW Pump Trip Throttle
        Valve.' Revision 00200. This step provides instructions for a 'slow start' of the
        TDAFW pump manually, following an overspeed trip of the pump, by using the
        trip throttle valve. This allows for starting of the pump even if the governor control
        valve is stuck in the full open position following the overspeed trip. This
        procedure step was successfully used following both the May 26th failure and
        the July 2nd failure. Per Operations management, the shift managers, who
        would be directing use of this procedure, were briefed on the updated procedure
        to ensure they were aware that new step was available for use and understood
        how it was to be performed. A controlled copy of the procedure is located at the
        TDAFW pump for use by the operator. Since this procedure was in effect prior
        to the July failure exposure period (Le., prior to the last successful TDAFW pump
        test on June 25, 2009), it is considered as a recovery for failures of the TDAFW
        pump.
Recovery actions identified in #1 above were not quantified by the team however the
evaluation approach appears to be appropriate. Prior to the licensee crediting recovery
actions identified in #2 above, the team was able to verify that the procedures were in
                                                                                    Enclosure
 
                                                12
    place and observed troubleshooting video in which the licensee started the TDAFW
    pump with this method. As a result the SRA concluded that the licensee's modeling
    demonstrating a risk reduction was appropriate.
    Based upon the close comparison between NRC and Constellation risk estimates, no
    sensitivity analyses were warranted. The use of V2 to approximate the exposure time
  was determined to be appropriate for standby or periodically operated components that
  fail due to a degradation mechanism that gradually affects the component during the
    standby time period. Inclusion of the unavailability time hours, due to troubleshooting
  and repairs, is also appropriate and consistent with the guidance promulgated in Risk
  Assessment of Operational Events Handbook, Revision 1.01, dated January 2008.
  This finding has a cross-cutting aspect in the area of Problem Identification and
    Resolution, Corrective Action Program, because Ginna did not implement a corrective
  action program with a low threshold for identifying issues completely, accurately, and in
  a timely manner commensurate with their safety significance. Specifically, Ginna did not
  identify issues associated with corrosion of the governor control valve within the
  corrective actions program. The inspectors concluded that the performance deficiency is
  reflective of current performance because Ginna had reasonable opportunities to identify
  the issue during troubleshooting in December 2008 and May 2009. [P.1(a) per IMC
  0305]
  Enforcement: 10 CFR 50, Appendix B, Criterion XVI, "Corrective Actions," states, in
  part, "Measures shall be established to assure that conditions adverse to quality, such
  as failures, malfunctions, defiCiencies, deviations, defective material and eqUipment, and
  nonconformances are promptly identified and corrected. In the case of significant
  conditions adverse to quality, the measures shall assure that the cause of the condition
  is determined and corrective action taken to preclude repetition." Contrary to the above,
  after identifying corrosion on the TDAFW pump governor control valve stem on April 11,
  2005, which is a significant condition adverse to quality, Ginna did not take adequate
  measures to determine the cause and prevent recurrence. The cause of the condition
  was left uncorrected and resulted in additional stem corrosion that led to binding of the
  governor control valve and the failure of the TDAFW pump on July 2, 2009. In addition,
  stem corrosion was the likely cause of the TDAFW pump failure on May 26, 2009. This
  issue was entered into Ginna's CAP as CR-:2009-003680 and CR-2009-004577.
  Pending final determination of significance, this finding is identified as an AV. (AV
  0500024412009008*01: Inadequate Corrective Actions Associated with the TDAFW
  Pump Governor Control Valve)
2. Untimely Corrective Actions Associated with Steam Admission Valves
  Introduction: A self-revealing NeVof 10 CFR 50, Appendix B, Criterion XVI, "Corrective
  Actions," was identified for the failure to establish adequate measures to correct a
  longstanding issue associated with steam a(]mission valves leakage. As a result, the
  leakage most likely contributed to the build-up of corrosion on the TDAFW pump
  governor control valve stem on May 26, 2009 and contributed to the failure of the
  TDAFW pump on July 2, 2009.
  Description: During a review of failures associated with the TDAFW pump, the
  inspectors noted that the steam admission valves had a history of leaking. Based on a
  review of the RCA report, industry operating experience, and associated CRs, the
                                                                                      Enclosure
 
                                            13
inspectors determined that the steam admission valve leakage was a contributing factor
in the development of corrosion of the governor control valve and contributed to the
failure of the TDAFW pump on July 2, 2009, and most likely the failure of the TDAFW
pump overspeed trip failure on May 26, 2009. Based on a review of eRs and interviews
of personnel, the inspectors determined that the steam admission valves had been
leaking since at least 2005.
In July 2005, CR-2005~3660 documented that steam admission valve 3505A was
leaking past its seat. However, Ginna did not take or plan any corrective actions
associated with the issue. By October 2006, steam admission valve 3505A leakage had
increased such that the TDAFW pump turbine was rotating approximately 100 rpm.
Ginna cycled the valve to reduce seat leakage, generated a work order to repair the
valve in May 2008, and conducted an evaluation of past operability. Ginna concluded
that there was no potential for increased consequences with time if the condition
continued. During the May 2008 refueling outage, Ginna conducted a repair of steam
admission valve 3505A. However, this corrective action was not effective; by September
2008, the valve was leaking again although at a reduced rate. The inspectors
determined that Ginna did not recognize or consider the potential impact of the steam
admission valve leakage on the governor control valve stem.
Immediate corrective actions included entering this condition in the CAP, replacing the
govemor control valve stem, and conducting weekly monitOring of the governor control
valve during surveillance te~ting to identify any potential for stem binding. Additionally,
the steam admission valves were inspected and re-worked and the govemor control
valve was Inspected during the fall 2009 outage. Ginna will continue to monitor the
governor control valve under an enhanced TDAFW surveillance program to ensure
TDAFW pump operability. Planned corrective actions include replacing the stem
admission valves in May 2011.
Analysis: The performance deficiency is that Ginna did not adequately address
deficiencies associated with steam admission valve leakage in that the leakage likely
resulted in accelerated corrosion of the governor control valve and contributed to the
failure of the TDAFW pump. The finding is more than minor because it is associated
with the equipment performance attribute of the Mitigating Systems cornerstone and
affects the cornerstone objective to ensure the availability and reliability of systems that
respond to initiating events to prevent undesirable consequences. Specifically, leakage
through the steam admission valves can res.ult in continuous wetting of the governor
control valve stem and lead to or accelerate corrosion of the governor control valve.
This could result in a stem binding of the govemor control valve and failure of the
TDAFW pump. The inspectors evaluated the significance of this finding using IMC 0609,
Attachment 4, "Phase 1 -Initial Screening and Characterization of Findings." The
finding is of very low safety significance because it is not a design or qualification
deficiency, did not represent a loss of a safety function of a system or a single train
greater than its TS allowed outage time, and did not screen as potentially risk Significant
due to external events. The inspectors determined that the steam admission valve
leakage was not a direct cause of the failure of the TDAFW pump overspeed events.
The steam admission valve leakage was a contributing factor in the development of
governor control valve stem corrosion and contributed to the failure of the TDAFW
pump.
                                                                                    Enclosure
 
                                                14
    This finding has a cross-cutting aspect in the area of Problem Identification and
    Resolution, Corrective Action Program, because Ginna did not thoroughly evaluate
    problems such that the resolutions address causes and extent of conditions, as
    r:eecessary, in a timely manner, commensurate with their significance. Specifically,
    Ginna did not thoroughly evaluate the potential effect of the steam admission valve
    leakage on the governor control valve performance. The inspectors determined that this
    issue is reflective of current licensee performance because each time the issue was
    identified and a CR was generated represented an opportunity for Ginna to adequately
    evaluate the issue and assign appropriate corrective actions. [P.1 (c) per IMC 0305]
    Enforcement: 10 CFR Part 50, Appendix B, Criterion XVI, "Corrective Actions," states, in
    part. "Measures shall be established to assure that conditions adverse to quality, such
    as failures, malfunctions, deficiencies, deviations, defective material and equipment, and
    nonconformances are promptly identified and corrected." Contrary to this requirement,
    from at least July 2005 to July 2, 2009, Ginna did not established adequate measures to
    correct longstanding steam admission valves leakage and/or minimize the impact of the
    leakage on the TDAFW pump governor control valve performance. As a result, leakage          I*
                                                                                                I
    through the steam admission valves contributed to the corrosion of the governor control
    valve and contributed to the failure of the TDAFW pump on July 2, 2009 and most likely
    the failure of the TDAFW pump on May 26, 2009. Because this violation is of very low
    safety significance (Green) and Ginna entered this issue into their CAP for resolution as
    CR-2009-003680 and CR-2009-004577, this violation is being treated as an NCV
    consistent with the NRC Enforcement Policy. (NCV 0500024412009008-02: Inadequate
    Corrective Actions Associated with Stearn Admission Valve Leakage)
2.2  Review of Operating Experience
a.  Inspection ScoQe
      The team reviewed operating experience involving TDAFW pump failures and actions
      taken by the Ginna staff to identify and address these types of failures. In addition, the
      team examined the specific issues associated with governor control valve stem binding
      to assess any new generic issues of industry interest for prompt communication and
      dissemination. As part of this evaluation, the inspectors reviewed pertinent industry
      operating experience, Ginna's response to NRC Information Notices, and interviewed
      key plant personnel.
b. Findings and Observations
    No Findings of Significance Identified.
    The inspectors determined that there were no new generic issues identified as a result of
    this event. However, the inspectors noted that Ginna missed opportunities to utilize
    industry operating experience to identify precursors associated with this event and to
    conduct effective troubleshooting. Specifically, following the discovery of corrosion on
    the exposed portion of the TDAFW pump govemor control valve stem in May 2005,
    Ginna did not enter this issue in to their CAP. As a result Ginna missed an opportunity
    to revisit operating experience from NRC IN 94-66 conceming governor control valve
    stem binding. In several examples in NRC IN 94-66, sites that experienced governor
    control valves stem binding identified stem corrosion following valve disassembly. Ginna
                                                                                      Enclosure
 
                                                15
    had originally determined that NRC IN 94-66 was not applicable to Ginna because the
    governor control valve was of a different configuration and material as those discussed
    in the IN and that corrosion of the stem had not been previously identified. Although this
    may have been a reasonable assessment during the original review of the NRC IN 94-66
    in 1994, the inspectors determined that once corrosion of the stem was identified in'May
    2005, Ginna missed an opportunity to revisit this operating experience. In addition, as
    discussed in Section 2.1.2 of this report. Ginna did not utilize Industry operating
    experience in evaluating a condition associated with steam admission valve leakage.
    NRC IN 94-66, other industry operating experience, and the vendor technical manual
    stated that steam admission valve leakage is a cause related to governor control valve
    stem binding. However, Ginna did not consider the impact of steam admission valve
    leakage on the governor control valve performance. Finally, the inspectors noted that
    Ginna missed opportunities to incorporate industry operating experience during
    troubleshooting efforts during the May 2009 TDAFW pump failure. NRC IN 94-66
    discussed several examples where a freedom of motion test was performed to test for
    stem binding with the governor control valve linkage disconnected and hydraulics not
    applied. However, during the May 2009 event, Ginna missed an opportunity to conduct
    this test and consequently, missed an opportunity to potentially identify the failure mode
    prior to the July 2, 2009, overspeed trip. Ginna captured these issues in their CAP
    under CR-2009-003680 and CR-2009-004577..
2.3 Review of Root Cause and Extent-ot-Condition
a. Inspection Scope
    The team evaluated the adequacy of Ginna's RCA and completed interim corrective
    actions. In addition the team evaluated the adequacy of Ginna's initial extent of
    condition for the TDAFW pump failures. The team reviewed plant drawings, procedures,
    and associated system modifications. In addition, the team conducted a walkdown of
    the TDAFW system and interviewed key Ginna personnel.
b. Findings and Observations
    Introduction: The inspectors identified an NCV of 10 CFR 50, Appendix B, Criterion III,
    "Design Control," for the failure to establish measures to ensure that a modification
    performed on the governor control valve bushing was a suitable application of materials
    for the TDAFW pump.
    Description: During the troubleshooting and repair of the TDAFW pump in July 2009,
    Ginna incorrectly evaluated that a vendor service bulletin allowed for larger stem-to
    bushing clearance than was prescribed in their current technical documents. Since
    there was overlap between the station technical information and the vendor service
    bulletin, Ginna decided to increase the clearance, by lapping the bushings, to reduce the
    likelihood that corrosion products would cause the stem to bind. To increase the
    clearance, Ginna removed some of the hardened layer on the bushing. During a review
    of the RCA, the inspectors determined that Ginna did not consider the potential impact of
    removing some ot the hardened layer on the corrosion rate of the governor control valve.
    The inspectors noted that by removing some of the hardened layer, the material property
    of the bushing could have been changed and/or additional micro-cracks could have been
    created or exposed that could increase the corrosion rate or potentially cause other
                                                                                      Enclosure
 
                                              16
problems such as stem-to~bushing galling. The inspectors noted that if the corrosion
rate is greater than predicted, then planned corrective actions may not be adequate to
maintain the TDAFW pump operable. Additionally, the team was concerned, that by
increasing the stem to bushing clearances, the stem would be susceptible to larger
steam exposure and that this could further accelerate the corrosion. Following concerns
raised by the inspectors, Ginna initiated CR-2009-005959 to ensure that all possible
consequences of lapping the TDAFW pump control valve bushing were fully evaluated.
In addition, Ginna assigned corrective actions to inspect the control valve bushing during
the fall 2009 refueling outage. During performance of the refueling inspection under WO
C90623685, pitting of the stem and corrosion of the bushings were observed.
Constellation initiated CR~2009-006765 and noted that the corrosion of the bushings
appeared to have been caused by the lapping of the bushing to achieve the desired
clearance between the stem and the bushings. The development of corrosion on the
bushing reduced the margin that was predicted to ensure adequate stem movement.
Immediate corrective actions following the inspection of the governor control valve
during the fall 2009 refueling outage included entering this condition in the CAP and
refurbishing the governor control valve with a new stem and bushing.
Analysis: The performance deficiency is that Ginna failed to establish measures to
ensure that a modification performed on the governor control valve bushing was a
suitable application of materials for the TDAFW pump. The finding is more than minor
because it is associated with the equipment performance attribute of the Mitigating
Systems cornerstone and affects the cornerstone objective to ensure the availability and
reliability of systems that respond to initiating events to prevent undesirable
consequences. Specifically, lapping of the valve bushing resulted in an unanticipated
corrosion mechanism of the governor control valve that impacted the reliability of the
TDAFW pump. The inspectors evaluated the Significance of this finding using IMC 0609,
Attachment 4, "Phase 1 -Initial Screening and Characterization of Findings." The
finding is of very low safety significance because it is not a design or qualification
deficiency, did not represent a loss of a safety fUnction of a system or a single train
greater than its TS allowed outage time, and did not screen as potentially risk significant
due to external events.
The inspectors determined that this finding has a cross-cutting aspect in the area of
Human Performance, Decision Making, because Ginna did not make a safety-significant
or risk-significant decision using a systematic process, especially when faced with
uncertain or unexpected plant conditions, to ensure safety was maintained. Specifically,
Ginna did not use a systematic process such as an engineering evaluation to properly
evaluate the potential impact of removing some of the hardened layer of the bushing.
[H.1(a) per IMC 0305]
Enforcement: 10 CFR 50, Appendix B, Criterion III, "Design Control" states, in part,
"Measures shall also be established for the selection and review for suitability of
application of materials, parts, equipment, and processes that are essential to the safety
related functions of the structures, systems and components." Contrary to the
requirements, in July 2009, Ginna failed to establish measures to ensure that a
modification performed on the governor control valve bushing was a suitable application
of materials for the TDAFW pump. Specifically, lapping of the valve bushing resulted in
an unanticipated corrosion mechanism of the governor control valve that had the
                                                                                    Enclosure
 
                                                  17
      potential to impact the performance of the TDAFW pump if not corrected. Because this
      violation is of very low safety significance (Green) and Ginna entered this issue into their
      CAP for resolution as CR-2009-006765, this violation is being treated as an NCV
      consistent with the NRC Enforcement Policy. (NeV 05000244/2009008-03: Failure To
      Establish Design Control Measures Associated With The Turbine Driven Auxiliary
      Feedwater Pump Governor Control Valve)
2.4  Risk Assessment of the As-Found Condition
  a.  Insoection Scope
      Prior to the initiation of the Special Inspection Team, the Region I SRA performed a
    CCDP assessment which conservatively bounded the potential risk significance of the
    degraded condition, assuming the TDAFW pump would fail to star on demand to
    mitigate the consequences of an event. The initial CCDP estimate was performed in
    accordance with IMC 0309, "Reactive Inspection Decision Basis for Reactors." The SRA
    used the Ginna SPAR model and associated GEM to evaluate the potential risk
    significance of this condition. The results of the IMC 0309 assessment are documented
    in report section 2.1.b.1 above.
b.  Final Risk Estimate
    Following team review and independent verification of the degraded turbine driven
    auxiliary feed water pump governor control valve, the team concluded that for
    approximately 119B hours, the TDAFW pump would not have been capable of
    responding to an event. Consistent with IMC 0609 conditional core damage probability
    assessment methodology, this degraded condition resulted in a loss of operability or
    safety function, and therefore was of low to moderate (B.6E-6) safety significance.
4.  OTHER ACTIVITIeS
40A6 Meetings, Including Exit
    On August 27 and on October 7,2009 the team presented the inspection results to Mr.
    John Carlin and other members of the R. E. Ginna Nuclear Power Plant staff. The
    inspectors verified that none of the materiall~xamined during the inspection is
    considered proprietary in nature.
                                                                                      Enclosure
 
                                                A-1
                                        ATTACHMENT A
                                  SUPPLEMENTAL INFORMATION
                                    KEY POINTS OF CONTACT
Licensee personnel
J. Carlin, Site Vice President
E. Larson, Plant General Manager
D. Crowley, Senior Engineer
E. Durkish, Associate Engineer
R. Everett, Supervisor, Primary Systems Engineering
T. Harding, Director, Licensing
R. Ruby, Principal Engineer, Licensing
P. Swift, Engineering Manager
                      LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
Opened
05000244/2009008-01                  AV            Failure to Preclude Recurrence of a
                                                    Significant Condition Adverse to Quality
                                                    Associated with the Turbine Driven Auxiliary
                                                      Feedwater Pump Governor Control Valve.
                                                    (Section 2.1.1)
Opened/Closed
05000244/2009008-02                    NCV          Inadequate Corrective Actions Associated
                                                    with Steam Admission Valve Leakage.
                                                    (Section 2.1.2)
05000244/2009008-03                    NCV          Failure to Establish Design Control
                                                    Measures Associated with the Turbine
                                                    Driven Auxiliary Feedwater Pump Governor
                                                    Control Valve. (Section 2.3)
                                I.IST OF DOCUMENTS REVIEWED
In addition to the documents identified in the body of this report, the inspectors reviewed the
following documents and records:
Corrective Actions
CA-2009-002311
Condition Reports
CR-2003-2006                CR-2005-3660            CR-2006-006029              CR-2006-006341
CR-2005-1509                CR-2005-5513            CR-2006-006204              CR-2006-006962
                                                                                      Attachment A
 
                                          A-2
CR-2007-000876        CR-2008-009911        CR-2009-004590          CR-2009-005959*
CR-2007-001302        CR-2009-003680        CR-2009-004591          CR-2009-006765*
CR-2008-003687        CR-2009-004222*      CR-2009-005964
CR-2008-007541        CR-2009-004577
*NRC Identified During Inspection
Corrective Action Tracking System
CATS R007325
Procedures
AP-FVV.1, Abnormal MFW Pump Flow or NPSH, Revision 01702
PT-16QT-T, Auxiliary Feedwater Turbine Pump - Quarterly, Revision 05900
CNG-MN-1.01-1002, Troubleshooting, Revision 0001
CNG-CA-1.01, Corrective Action Program, Revision 0001
CNG-CA-1.01-1004, Root Cause Analysis, Revision 0001
CNG-CA-1.01-1005, Apparent Cause Evaluation, Revision 0100
CNG-CA-1.01-1006, Common Cause Analysis, Revision 0001
CNG-CA-1.01-1007, Trending, Revision 0000
CNG-CA-1.01-1010, Use of OE, Revision 0000
IP-CAP-1, Ginna Condition Reporting, Revision 02800
M-11.5C, Auxiliary Feedwater Pump Motor Mechanical Inspection and Maintenance,
      Revision 03000
0-1.1, Plant Heatup From Cold Shutdown to Hot Shutdown, Revision 16301
PT-16Q-T, Auxiliary Feedwater Turbine Pump - Quarterly, Revision 05600. Completed
3/14/08,514108,5/5/08,6/11/08,9/4/08, 1213/08, 1214/08, 12111/08, 12/18/08,2/12/09,
5/26/09, 5/28/09
Surveillance Tests
PT-16Q-T, Auxiliary Feedwater Turbine Pump - Quarterly, Revision 05600, 03/14/2008
PT-16Q-T, Auxiliary Feedwater Turbine Pump -. Quarterly, Revision 05700, 05/04/2008
PT-16Q-T, Auxiliary Feedwater Turbine Pump _. Quarterly, Revision 05700,05/05/2008
PT-16Q-T, Auxiliary Feedwater Turbine Pump - Quarterly, Revision 05700. 06/11/2008
STP-0-16-COMP-T, Auxiliary Feedwater Turbine Pump - Comprehensive Test,
        Revision 00000, 06/11/2008
PT-16Q-T, Auxiliary Feedwater Turbine Pump - Quarterly. Revision 05701, 09/03/2008
PT-16Q-T, Auxiliary Feedwater Turbine Pump - Quarterly, Revision 05701, 12/02/2008
PT-16Q-T, Auxiliary FeedwaterTurbine Pump - Quarterly. Revision 05701,12103/2008
PT-16Q-T. Auxiliary Feedwater Turbine Pump _. Quarterly, Revision 05701, 12/04/2008
PT-16Q-T, Auxiliary Feedwater Turbine Pump _. Quarterly, Revision 05702, 12/11/2008
PT-16Q-T, Auxiliary Feedwater Turbine Pump _. Quarterly, Revision 05702, 12/18/2008
PT-16Q-T, Auxiliary Feedwater Turbine Pump - Quarterly, Revision 05801, 01116/2009
PT-16Q-T, AUXiliary Feedwater Turbine Pump - Quarterly, Revision 05801, 02112/2009
PT-16Q-T, AUXiliary Feedwater Turbine Pump _. Quarterly. Revision 05900,05/26/2009
PT-16Q-T, Auxiliary Feedwater Turbine Pump - Quarterly, Revision 05900,05/28/2009
STP-0-16-COMP-T, Auxiliary Feedwater Turbine Pump - Comprehensive Test,
        Revision 00400, 05/28/2009
                                                                            Attachment A
 
                                          A-3
Work Orders
W020604989
W020401907
Drawings
DWG No. 33013-1231, Main Steam System, Revision 37
DWG No. 33013-2285, Motor Driven and Turbine Driven Auxiliary Feedwater Pumps
      Lube Oil Skid, Revision 17
DWG No. LB-112541, Turbine Control and Quick Start System
DWG No. T040-001A, TDAFW Control Oil System, Revision 0
DWG No. T040-002A, TDAFW Turbine Trip Valve, Revision 0
DWG No. T040-003A, Auxiliary and Standby Aux. Feedwater Systems, Revision 2
DWG No. T040-003B, SAFW System 1-Line Diagram, Revision 0
DWG No. T040-003C, AFW System 1-Une Diagram, Revision 1
DWG No. T040-004A, Auxiliary Feedwater Pump Auto Start Signals, Revision 0
DWG No. T830-004A, Blowdown Isolation Solenoid Control Circuit, Revision 0
Other Documents
Vendor Report, Preliminary Results ofStem Sticking Failure Mechanisms, July 20, 2009
Vendor Report 09-1929 Part 1, Equipment Root Cause Analysis of AFWP Control Valve
      Stem Sticking Problem at Ginna Nuclear Power Station
Vendor Technical Question Response, August 26, 2009
Category I Root Causal Analysis, May and July 2009 Turbine Driven Auxiliary Feedwater
      Pump (TDAFWP) Failures; Overspeed Trip During Testing
vrD-E9016-4001, Excerpts from EPRI Manual 1007461, Terry Turbine Maintenance
      Guide, AFW Application, Revision 000
vrD-G0153-4001, Operating Instructions Easy Flow Body Combined Trip Throttle Valve,
      Revision 2
VrD-W0315-4001, Instructions For 465 H.P. Non-Condensing Steam Turbine Serial
      Number 26635, Revision 000
VrD-W0315-4002, Service Department Standards Book No. 10, Field Service Manual,
      Revision 000
Response to NRC Generic Letter 90-3, Relaxation of Staff Position In Generic Letter 83
      28, Item 2.2 Part 2 "Vendor Interface for Safety Related Components, dated
      September 18, 1990
CATS 10 R04451, Response to NRC IN 94-66, OVERSPEED OF TURBINE-DRIVEN
      PUMPS CAUSED BY GOVERNOR VALVE STEM BINDING
CMM-37-19-9519E, Worthington Turbine Driven Auxiliary Feedwater Pump Hydraulic
      Governor Control Valve Maintenance for 9519E, Revision 00200
Constellation Energy Nuclear Generating Group Reply to a Notice of Violation; EA-09
      045
Engineering Change Package No. ECP-2009-0146, TDAFW Lube Oil Orifice
Management Review Committee Agenda. August 5, 2009
Purchase Requisition No. 58686, Dresser-Rand Valve Stem
Technical Staff Request 97-199, Leakoff from TDAFW Govenor Valve 9519E
Management Review Committee Agenda, August 5, 2009
Purchase Requisition No. 58686, Dresser-Rand Valve Stem
                                                                          Attachment A
 
                                          A-4
Technical Staff Request 97-199, Leakofffrom TDAFW Govenor Valve 9519E
Turbine Driven Auxiliary Feedwater Pump Preventive Maintenance Strategies
Auxiliary Feed Water System, 1st Quarter 200S
Auxiliary Feed Water System. 2nd Quarter 200S
Auxiliary Feed Water System. 3rd Quarter 200S
Auxiliary Feed Water System, 4th Quarter 200S
Auxiliary Feed Water System, 1st Quarter 2009
Operating Experience
OE-200S-000397
OE-200S-000607
OE-200S-000847
oE-20OS-00S60
OE-2008-001296
OE-2009-00212
OE*2009*001178
Oil Analysis
Pump IB Oil Analysis. 2008-03
Pump OB Oil Analysis, 2008-03
Reservoir Oil Analysis 2008-05
Reservoir Oil Analysis 2008-08
Reservoir Oil Analysis 2009-05
                                                                      Attachment A
 
                              A-4
                    LIST OF ACRONYMS
  AV    Apparent Violation
  CAP  Corrective Action Program
  CCDP  Conditional Core Damage Probability
  CDF  Core Damage Frequency
  CR    Condition Report
  DRP  Division of Reactor Projects
  EDG  Emergency Diesel Generator
  GEM  Graphical Evaluation Module
  ICCDP Incremental Conditional Core Damage Probability
  IMC  Inspection Manual Chapter
  IN    Information Notice
  INL  Idaho National Labs
*IPEEE  Individual Plant Examination of External Events
  LERF  Large Early Release Frequency
  LOOP  Loss of Offsite Power
  LOSWS Loss of Service Water System
  NCV  Non Cited Violation
  NRC  Nuclear Regulatory Commission
  NRR  Office of Nuclear Reactor Regulation
  PARS  Publicly Available Records
  PSA  Probabilistic Safety Assessment
  RCA  Root Cause Analysis
  SAFW  Standby Auxiliary Feedwater
  SBO  Station Blackout
  SOP  Significance Determination Process
  SPAR  Standardized Plant Analysis Risk
  SRA  Senior Reactor Analyst
  SCAQ  Significant Condition Adverse to Quality
  NCV  Non-citied Violation
  TBD  To Be Determined
TDAFW  Turbine Driven Auxiliary Feedwater
TS    Technical Specification
                                                        Attachment A
 
                                                8-1
                                  Special Inspection Charter
                                R.E. Ginna Nuclear Power Plant
            Failure of the Turbine-Driven Auxiliary Feedwater (TDAFW) Pump
                              on May 26, 2009 and July 2, 2009
Background:
On May 26, 2009, during routine quarterly surveillance testing of the turbine driven
auxiliary feedwater (TDAFW) system, the TDAFW pump tripped on overspeed. The test
was repeated several hours later and the TDAFW pump tripped again on overspeed.
Fluctuations in oil pressure were observed during the testing.
After extensive troubleshooting, Ginna personnE~1 identified a number of issues but no
definitive cause for the overspeed trips. The lube/control oil system was drained and
cleaned due to the presence of fine particulates; a pressure pulsation dampener
accumulator bladder was replaced due to a below normal pressure condition; the oil
pressure regulating bypass valve was replaced due to potential cycling; a change to
linkage setup was implemented; governor relay valve, and trip and throttle valve parts
were replaced due to out of specification clearances; and a miSSing oil line orifice was
installed. Following these corrective actions, the system was successfully tested and
declared operable.
Constellation is completing a root cause evaluation and the resident inspectors continue
to conduct baseline inspections with assistance from DRS specialists. Testing of the
TDAFW system will be at an increased frequency until Constellation has confidence that
the system is performing as required.
On July 2, 2009, during the performance of the increased frequency surveillance, the
TDAFW pump again tripped on overspeed. Glnna personnel discovered pitting and
corrosion on the stem of the governor control valve during troubleshooting activities to
restore the pump to operable status. This Special Inspection Team had raised concerns
regarding corrosion on the stem of the Governor Control Valve during onsite inspection
activities the week of June 15, 2009.
Basis for the Formation of the SIT:
The failure of the TDAFW pump involved repetitive failures of this safety~related
eqUipment. There have been three failures of the TDAFW pump since December 2008.
On December 2, 2008, a failure was attributed to inadequate implementation of the
preventive maintenance program. SpeCifically, the governor linkages were not
lubricated in March 2008 which resulted in the pump's inability to achieve the required
flow and pressure in December 2008. On July 2, 2009, the failure was preliminarily
determined to be caused by pitting on the stem of the Governor Control valve and overly
tolerances causing binding of the stem. Although the specific failure modes (overspeed
trip, inability to achieve the required flow or pressure) were different, the underlying
cause of inadequate or inappropriate preventive maintenance may be the same.
                                                                                Attachment 8
 
                                              B-2
Based upon best available information, the Region I Senior Reactor Analyst (SRA)
conducted a preliminary risk estimate of the May 26 TDAFW pump failure. An
incremental conditional core damage probability (ICCDP) in the upper E-6 range (8E-6
per the 82 day exposure period), was calculated using the Ginna SPAR model.
assuming that the TDAFW pump would not have started since the last time it passed a
surveillance test on March 5 until May 26 (82 days). The dominant core damage
sequence was a station blackout (LOOP with failure of both EDGs,) with no TDAFW and
failure to recover offsite power or an EDG in one hour.
Based upon the preliminary conditional core damage probability estimate of upper E-6
range, in accordance with IMC 0309, this event falls within the region for a Special
Inspection Team.
Oblectives of the Special Inspection:
The objectives of the special inspection are to review and assess: (1) Constellation's
planning and execution of the risk significant work activities on the TDAFW system; (2)
equipment issues related to the TDAFW testing; and (3) Constellation's response to this
significant equipment failure.
To accomplish these objectives, the following will be performed:
    1. Evaluate the adequacy and completeness of the maintenance on the TDAFW
          system, including preventive maintenance, procedural guidance, post
          maintenance testing, and supervisory oversight.
    2. Evaluate Constellation's application of pertinent industry operating experience
          and evaluation of potential precursors, including the effectiveness of any actions
          taken in response to the operating experience or precursors.
    3. Evaluate the adequacy of Constellation's response to the TDAFW system
        failures, including Constellation's cause analysis and completed interim corrective
        actions.
    4. Evaluate the adequacy of Constellation's initial extent of condition for the TDAFW
        failures, as appropriate.
    5. Evaluate the failure modes for potential generic implications including the need
        for generic communications
Additionally, the team leader will review lessons learned from the Special Inspection
and, if appropriate, prepare a feedback form on recommendations for revising the
reactor oversight process (ROP) baseline inspection procedures in order to proactively
identify the issues and causes involved with the event.
Guidance:
Inspection Procedure 93812, "Special Inspection", provides additional guidance to be
used by the Special Inspection Team. Team duties will be as described in Inspection
Procedure 93812. The inspection should emphasize fact-finding in its review of the
circumstances surrounding the event. It is not the responsibility of the team to examine
                                                                              Attachment B
 
                                            8-3
the regulatory process. Safety concerns identified that are not directly related to the
event should be reported to the Region I office for appropriate action.
The Team will conduct an entrance meeting and begin the inspection on June 8,2009.
While on site, the Team Leader wi" provide daily briefings to Region I management, who
will coordinate with the Office of Nuclear Reactor Regulation, to ensure that all other
parties are kept informed. A report documenting the results of the inspection should be
issued within 45 days of the completion of the inspection.
This Charter may be modified should the team develop significant new information that
warrants review.
                                                                            Attachment 8
}}
}}

Latest revision as of 01:36, 14 November 2019

IR 05000244-09-008; 06/15/2009 - 06/19/2009 and 08/24/2009 - 08/27/2009; R. E. Ginna Nuclear Plant; Special Inspection Team Report
ML093160122
Person / Time
Site: Ginna Constellation icon.png
Issue date: 11/12/2009
From: David Lew
Division Reactor Projects I
To: John Carlin
Ginna
Clifford J
References
EA-09-249 IR-09-008
Download: ML093160122 (29)


See also: IR 05000244/2009008

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION I

475 ALLENDALE ROAD

KING OF PRUSSIA, PA 19406-1415

November 12, 2009

EA-09-249

Mr. John T. Carlin

Vice President, RE. Ginna Nuclear Power Plant

RE. Ginna Nuclear Power Plant, LLC

1503 Lake Road

Ontario, New York 14519

SUBJECT: RE. GINNA NUCLEAR POWER PLANT - NRC SPECIAL INSPECTION TEAM

REPORT 05000244/2009008; PRELIMINARY WHITE FINDING

Dear Mr. Carlin:

On June 16-20, 2009, and August 24-27,2009, the U.S. Nuclear Regulatory Commission (NRC)

conducted the onsite portions of a special inspection at RE. Ginna Nuclear Power Plant. In

office inspection reviews were conducted in the intervening weeks. The enclosed report

documents the inspection team's findings and observations which were discussed with you and

others members of your staff on August 27, 2009, during a preliminary exit briefing, and on

October 7, 2009, during the final exit meeting.

The special inspection was conducted in response to a turbine driven auxiliary feedwater

(TDAFW) pump overspeed trip on May 26, 2009. The team included a subsequent overspeed

trip on July 2,2009 into its inspection scope. The NRC's initial evaluation of this condition

satisfied the criteria in NRC Inspection Manual Chapter 0309, "Reactive Inspection Decision

Basis for Reactors," for conducting a special inspection. The basis for initiating this special

inspection is further discussed in the inspection team's charter that is included in this report as

Attachment B.

The inspection examined activities conducted under your license as they relate to safety and

compliance with the Commission's rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

This letter transmits one self-revealing finding that, using the reactor safety Significance

Determination Process (SOP), has preliminarily been determined to be White, a finding with low

to moderate safety significance. The finding is associated with the failure to preclude

recurrence of a significant condition adverse to quality associated with the corrosion of the

governor control valve of the turbine driven auxiliary feedwater (TDAFW) pump, that led to a

failure of the TDAFW pump during surveillance testing on July 2, 2009 and was the likely cause

of the overspeed trip on May 26, 2009. Following the July test failure, Ginna replaced the

J. Carlin 2

governor control valve stem and conducted weekly monitoring of the governor control valve

during surveillance testing to identify any potential for stem binding. In addition, corrective

actions included a follow-up inspection of the governor control valve during the fall 2009

refueling outage. There is no immediate safety concern present due to this finding because the

system is now operable and the long term corrective actions are being implemented in Ginna's

corrective action program. The final resolution of this finding will be conveyed in a separate

correspondence.

As discussed in the attached Inspection report. the tinding is also an apparent violation of NRC

requirements. specifically, 10 CFR Appendix B, Criterion XVI. "Corrective Actions." and is

therefore being considered for escalated enforcement action in accordance with the

Enforcement Policy, which can be found on the NRC's Web site at http://www.nrc.gov/reading

rm/doc-collections/enforcementl.

Following a discussion of the preliminary safety Significance of this finding during the initial exit

briefing on August 27,2009. a phone call was held between Glenn Dentel, Branch Chief,

Division of Reactor Projects. and yourself on October 1. 2009. During this call, you indicated

that R.E. Ginna Nuclear Power Plant does not contest the characterization of the rIsk

significance of this finding, and therefore you have declined to further discuss this issue at a

Regulatory Conference or provide a written response. Please note that by declining to request

a Regulatory Conference or submit a written response, you relinquished your right to appeal the

final SOP determination. in that by not doing either, you would not meet the appeal

requirements stated in the Prerequisite and Limitation sections of Attachment 2 of IMC 0609.

You will be advised by a separate correspondence of the results of our deliberations on this

matter.

In addition. the report documents two findings of very low safety significance (Green). The

findings involved violations of NRC requirements. However, because of the very low safety

significance and because they are entered into your corrective action program (CAP). the NRC

is treating these findings as non-cited violations (NeVs) consistent with Section VI.A.1 of the

NRC Enforcement Policy. If you contest any NCV in this report, you should provide a response

within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear

Regulatory Commission, A TIN.: Document Control Desk, Washington, DC 20555-0001; with

copies to the Regional Administrator, Region I; the Director, Office of Enforcement; and the

NRC Resident Inspector at R.E. Ginna. In addition. if you disagree with the characterization of

any finding in this report, you should provide a response within 30 days of the date of this

inspection report. with the basis for your disagreement, to the Regional Administrator, Region I,

and the NRC Resident Inspector at R.E. Ginna Nuclear Power Plant. The information you

provide will be considered in accordance with Inspection Manual Chapter 030?

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its

enclosure, and your response (if any) will be available electronically for public inspection in the

J. Carlin 3

NRC Public Document Room or from the Publicly Available Records (PARS) component of the

NRC's document system (ADAMS). ADAMS is accessible from the NRC Web Site at

http://www.nrc.gov/reading-rm/adams.html(the Public Electronic Reading Room).

Sincerely,

,/;I,/;tJ

D~ew,~~ --fbr-

Division of Reactor Projects

Docket No.: 50-244

License No.: DPR-18

Enclosures: Inspection Report 05000244/2009008

w/Attachment A: Supplemental Information

w/Attachment B: Special Inspection Charter

cc w/encl: Distribution via ListServ

J. Carlin 2

NRC Public Document Room or from the Publicly Available Records (PARS) component of the

NRC's document system (ADAMS). ADAMS is accessible from the NRC Web Site at

httg:llwww.nrc.gov/reading*rm/adams.html(the Public Electronic Reading Room).

Sincerely,

IRAJ James W. Clifford for:

David C. lew, Director

Division of Reactor Projects

Docket No.: 50-244

License No.: DPR-18

Enclosures: Inspection Report 05000244/2009008

w/Attachment A: Supplemental Information

w/Attachment B: Special Inspection Charter

cc w/encl: Distribution via ListServ

SUNSI Review Complete: gtd (Reviewer's Initials)

DOCUMENT NAME: G:\DRP\BRANCH1\Ginna\TDAFW SIT\AED Track Changes Ginna SIT

Report Rev 4 cC.doc

After declaring this document "An Official Agency Record" it will be released to the Public.

To receive I!I copy of this document, indicate in the box: "C' =Copy without attachmenVenclosure "e" = Copy with

attaclhmentlenclosure "N";:; No co ML093160122

OFFICE RI/DRS RI/ENF RI/DRP

NAME CCahill/cc* JClifford/jwc

DATE 10/21109 11/05/09

  • see prior concurrence OFFICIAL RECORD COpy

Distribution w/encl:

S. Collins, RA (R10RAMaii Resource) ROPreports@nrc.gov

M. Dapas, ORA (R10RAMaii Resource)

D. Lew, DRP (R1DRPMaii Resource)

J. Clifford, DRP (R1DRPMail Resource)

l. Trocine, RI OEDO

RidsNrrPMREGinnaResource

RidsNrrDorlLpl1-1 Resource

G. Dentel, DRP

N. Perry, DRP

J. Hawkins, DRP

K. Kolaczyk, DRP, SRI

S. Kennedy, DRP, SRI

L. Casey, DRP, RI

M. Rose, DRP, OA

D. Bearde, DRP

1

U.S. NUCLEAR REGULATORY COMMISSION

REGION I

Docket No.: 50-244

License No.: DPR-18

Report No.: 05000244/2009008

Licensee: Constellation Energy, R. E. Ginna Nuclear Power Plant, LLC

Facility: R. E. Ginna Nuclear Power Plant

Location: Ontario. New York

Dates: June 15-19, 2009 and August 24-27.2009

Team Leader: C. cahill, Senior Reactor Analyst, Division of Reactor Safety

Inspectors: S. Kennedy, Senior Resident Inspector, Division of Reactor Projects

K. Kolaczyk, Senior Resident Inspector, Division of Reactor Projects

J. Bream, Project Engineer. Division of Reactor Projects

Approved by: Glenn T. Dentel, Chief

Projects Branch 1

Division of Reactor Projects

2

SUMMARY OF FINDINGS

IR 05000244/2009008; 06/15-19/2009 and 08/24-2'712009; R. E. Ginna Nuclear Plant; Special

Inspection Team Report.

The report covered two on-site inspection visits and related in-office inspection activities by a

special inspection team consisting of a Senior Reactor Analyst. two Senior Resident Inspectors.

and one Project Engineer. One apparent violation (AV) with potential for greater than Green

safety significance and two Green findings were identified. The significance of most findings is

indicated by its color (Green. White, Yellow, or Red) using Inspection Manual Chapter (lMC)

0609, "Significance Determination Process." Findings for which the significance determination

(SDP) process does not apply may be Green or be assigned a severity level after NRC

management review. The NRC program for overseeing the safe operation of commercial

nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 4,

dated December 2006.

NRC Identified and Self-Revealing Findings

Cornerstones: Mitigating Systems

Preliminary White: A self-revealing apparent violation (AV) of 10 CFR 50, Appendix B,

Criterion XVI, uCorrective Actions," was identified for the failure to preclude recurrence

of a signIficant condition adverse to quality (SCAQ) associated with the Turbine Driven

Auxiliary Feedwater (TDAFW) pump governor control valve. Specifically, after

identifying corrosion of the govemor control valve stem in April 2005, Ginna did not take

adequate corrective actions to preclude the recurrence of corrosion which led to the

binding of the gavemar control valve and failure of the TDAFW pump on July 2,2009.

In addition, the inspectors concluded that governor control valve stem binding was the

likely cause of the failure of the TDAFW pump on May 26,2009. The overspeed trip of

the TDAFW pump on May 26. 2009. was originally determined by Ginna to be failure of

the governor control system relay valve. Governor control valve stem corrosion is a

SCAQ because corrosion of the stem can IHad to governor control valve stem binding

and failure of the TDAFW pump as discussed in NRC Information Notice (IN) 94-66:

"Overspeed of Turbine-Driven Pumps Caused by Governor Valve Stem Binding" and

other related industry operating experience documents. Immediate corrective actions

inCluded entering this condition in the corrective action program (CAP). conducting a

root cause analysis (RCA). replacing the governor control valve stem, and conducting

weekly monitoring of the governor control valve during surveillance testing to identify

any potential for stem binding. In addition, corrective actions included a follow-up

inspection of the governor control valve during the fall 2009 refueling outage. Ginna will

continue to monitor the govemor control valve under an enhanced TDAFW surveillance

program to ensure TDAFW pump operability.

The finding is more than minor because it is associated with the equipment performance

attribute of the Mitigating System cornerstone and affects the cornerstone objective to

ensure the availability, reliability, and capability of systems that respond to initiating

events to prevent undesirable consequences. Specifically. stem corrosion caused

binding of the governor control valve and led to the failure of the TDAFW pump. This

finding was assessed using IMC 0609 and preliminarily determined to be White (lOW to

moderate safety significance) based on a Phase 3 analysis with a total (internal and

Enclosure

3

external contributions) calculated conditional core damage frequency (CCDF) of B.6E-6.

This finding has a cross-cutting aspect in the area of Problem Identification and

Resolution, Corrective Action Program, because Ginna did not implement a corrective

action program with a low threshold for identifying issues completely, accurately, and in

a timely manner commensurate with their safety significance P.1(a} per IMC 0305].

Specifically, Ginna did not identify issues a~;sociated with corrosion of the governor

control valve within the corrective action program. (Section 2.1.1)

Green: A self-revealing non-cited violation (NCV) of 10 CFR 50, Appendix B, Criterion

XVI, "Corrective Actions," was identified for the failure to establish adequate measures

to correct a longstanding issue associated with steam admission valves leakage. As a

result, the leakage most likely contributed to the build-up of corrosion on the TDAFW

pump governor control valve stem and contributed to the failure of the TDAFW pump on

May 26, 2009, and on July 2, 2009. The steam admission valves had been leaking

since at least 2005. However, G.inna did not take adequate measures to correct the

leakage or minimize the impact of the leakage on governor control valve performance.

Immediate corrective actions included entering this condition in the corrective action

program, conducting a root cause analysis, replacing the governor control valve stem,

and conducting weekly monitoring of the governor control valve during surveillance

testing to identify any potential for stem binding. Additionally, the steam admission

valves were inspected and re-worked and the governor control valve was inspected

during the fall 2009 outage. Ginna will continue to monitor the governor control valve

under an enhanced TDAFW surveillance program to ensure TDAFW pump operability.

Planned corrective actions include replacin~~ the steam admission valves in May 2011.

The finding is more than minor because it is associated with the equipment performance

attribute of the Mitigating Systems cornerstone and affects the cornerstone objective to

ensure the availability and reliability of systems that respond to initiating events to

prevent undesirable consequences. Specifically, leakage through the steam admission

valves can result in continuous wetting of the governor control valve stem and lead to or

accelerate corrosion of the governor control valve. This could result in a stem binding of

the governor control valve and failure of the TDAFW pump. The inspectors evaluated

the signifiCance of this finding using IMC 0609, Attachment 4, "'Phase 1 - Initial

Screening and Characterization of Findings." The finding is of very low safety

significance because it is not a design or qualification deficiency, did not represent a

loss of a safety function of a system or a single train greater than its technical

speCification (TS) allowed outage time, and did not screen as potentially risk Significant

due to external events. This finding has a cross-cutting aspect in the area of Problem

Identification and Resolution, Corrective Action Program, because Ginna did not

thoroughly evaluate problems such that the resolutions address causes and extent of

conditions, as necessary, In a timely manner, commensurate with their significance

[P.1 (c) per IMC 0305]. Specifically, Ginna did not thoroughly evaluate the potential

effect of the steam admission valve leakage on the governor control valve performance.

(Section 2.1.2)

Green: The inspectors identified an NCVof 10 CFR 50, Appendix B. Criterion III,

"Design Control," for the failure to establish measures to ensure that a modification

performed on the governor control valve bushing was a suitable application of materials

for the TDAFW pump. During a review of the RCA associated with the TDAFW pump

failures, the inspectors noted that Ginna did not consider the potential impact of

Enclosure

4

removing some of the hardened layer of the bushing on the corrosion rate of the

governor control valve. Following concerns raised by the inspectors, Ginna inspected

the governor control valve bushing during the fall 2009 refueling outage and observed

corrosion of the bushings. Ginna noted that the corrosion of the bushings appeared to

have been caused by the lapping of the bushing to achieve the increased clearance

between the stem and the bushings. Immediate corrective actions following the

inspection of the governor control valve during the fall 2009 refueling outage included

entering this condition in the CAP and refurbishing the governor control valve with a new

stem and bushing.

The finding is more than minor because it is associated with the equipment performance

attribute of the Mitigating System cornerstone and affects the cornerstone objective to

ensure the availability, reliability, and capability of systems that respond to initiating

events to prevent undesirable consequences. Specifically, lapping of the valve bushing

resulted in an unanticipated corrosion mechanism of the govemor control valve that

impacted the reliability of the TDAFW pump" The inspectors evaluated the significance

of this finding using IMC 0609, Attachment 4. "Phase 1 Initial Screening and

Characterization of Findings." The finding is of very low safety significance because it is

a design or qualification deficiency confirmed not to result in the loss of operability or

functionality. The inspectors determined that this finding has a cross-cutting aspect in

the area of Human Performance, Decision Making. because Ginna did not make a

safety-significant or risk-significant decision using a systematic process, especially when

faced with uncertain or unexpected plant conditions, to ensure safety was maintained

H.1(a) per IMC 0305]. Specifically, Ginna did not use a systematic process such as an

engineering evaluation to properly evaluate the potential impact of removing some of the

hardened layer of the bushing. [H.1 (a) per IMC 0305]

(Section 2.3)

Licensee Identified Violations

None

Enclosure

5

REPORT DETAILS

1. INTRODUCTION

1.1 Background and Event Description

On May 26, 2009, and July 2, 2009, the TDAFW pump tripped on overspeed during the

performance of surveillance testing activities. These were the second and third times

the TDAFW pump had failed a surveillance test in a six month period. The previous test

failure occurred on December 2, 2008, when the TDAFW pump failed to develop

acceptable discharge pressure during a quarterly surveillance test. Details surrounding

the December test failure including Ginna corrective actions are discussed in NRC

Integrated Inspection Report 50-244/2009002. Following each of the three test failures,

Ginna declared the TDAFW pump inoperable and entered the limiting Condition for

Operation for TS 3.7.5 "Auxiliary Feedwater."

Following the May 26, 2009, test failure, Ginna troubleshooting activities were focused

on the TDAFW lubricating oil system where system pressure oscillations were noted by

test personnel prior to the pump overspeed trip. As part of the troubleshooting efforts,

the TDAFW lubricating oil system was drained and refilled with fresh oil, filters in the

lubrication system were examined and replaced, and several components in the

lubricating oil system including the relay and pressure regulating valves were replaced.

Additionally the turbine governor linkage was adjusted to original specifications outlined

in the vendor technical documents. Although several out of speCification and missing

components were identified during this troubleshooting effort, a definitive cause for the

surveillance failure was not identified. Nevertheless, following the successful completion

of post maintenance testing activities, Ginna declared the TDAFW pump operable and

commenced an augmented surveillance testing program for the TDAFW pump that

tested the pump on a weekly basis.

On July 2, 2009, another TDAFW pump overspeed failure occurred when the pump was

undergoing the augmented testing program. Troubleshooting activities following this

failure were focused on the turbine control system, which did not appear to have

functioned properly during the test. Accordingly, the turbine control and relay valves

were disassembled and inspected, and the governor linkage system was adjusted.

Additionally. the lubricating oil system was flushed and examined for particulates.

However, unlike the May 26 failure, these troubleshooting activities identified a definitive

cause, a stuck governor control valve stem, that resulted in the surveillance test failure.

Visual inspection of the stem, which had become bound to its bushing and had to be

forcibly removed, revealed corrosion buildup where the stem contacted the upper valve

bushing. To restore the control valve to an operable status, Ginna replaced the valve

stem and increased the bushing clearances to dimensions specified by the Ginna

TDAFW pump inspection procedure. The pump was successfully tested and declared

operable subject to an augmented testing program.

Ginna assigned an RCA team to investigate the surveillance test failures. The Ginna

RCA team concluded that the primary root cause of the failure of the governor contrOl

valve to control turbine speed on July 2,2009, was binding caused by a corrosion

mechanism that occurred between the valve stem and the valve bushings. The RCA

team also concluded that stem binding appeared to be an intermittent problem and that

Enclosure

6

station members missed opportunities to identify the failure mode during previous

surveillances and failures. As such, the RCA team determined that governor control

valve stem binding could not be ruled out as a possible failure mode during the

December 2008 and the May 2009 TDAFW pump failures.

At Ginna's request, an independent vendor reviewed the issues associated with the

governor control valve stem binding to determine the failure mechanism that was the

cause of the TDAFW pump overspeed trips. The vendor determined that the most likely

cause of the corrosion of the governor control valve stem was fresh-water corrosion

(Langelier corrosion) that was the result of galvanic interactions between the nitrided

case and the base material of the governor control valve stem. The vendor considered

several variables that contributed to the corrosion mechanism such as material

composition of the stem and bushing, stem-to-bushing clearance, steam admission

valve leakage, and TDAFW pump surveillance frequency and duration.

1.2 Special Inspection Scope

The NRC conducted this inspection to gain a better understanding of the circumstances

involving the TDAFW pump overspeed trips during surveillance testing on May 26, 2009,

and on July 2,2009. The inspection team used NRC Inspection Procedure 93812,

"Special Inspection," as a guide to complete their review. Additional inspection and

review activities were outlined in the special inspection team charter, provided as

Attachment B. The special inspection team reviewed procedures, corrective action

documents, work orders, engineering analyses, and the root cause evaluation prepared

by Ginna. In addition. the team conducted equipment walkdowns and interviewed key

plant personnel regarding the discovery and resolution of the condition. A list of site

personnel interviewed and documents reviewed are provided in Attachment A to this

report.

1.3 Preliminary Conditional Risk Assessment

Using IMC 0309, "Reactive Inspection Decision Basis for Reactors," IMe 0609,

"Significance Determination Process," and the Ginna Standardized Plant Analysis Risk

(SPAR) model in conjunction with the Graphical Evaluation Module (GEM). the Region I

Senior Reactor Analyst (SRA) evaluated the increase in conditional core damage

probability for the failure of the TDAFW pump. Based on the nature of the failure and

the subsequent overspeed trip on an instrumented diagnostic run, the condition was

evaluated as being non-recoverable in the event of actual demand.

Based upon best available information, an incremental conditional core damage

probability (ICCDP) in the upper E-6 range (8E-6 per the 82 day exposure period), was

calculated. The exposure period was based on the assumption that the TDAFW pump

would not have started since the last time it passed a surveillance test on March 5 until

May 26 (82 days). The dominant core damage sequence was a station blackout (loss of

offsite power (LOOP) with failure of both emergency diesel generators (EDGs), with no

TOAFW and failure to recover offsite power or an EDG in one hour.

Based upon this conservative conditional core damage probability (CCDP) value, and

having satisfied an IMC 0309 deterministic criterion, the May 26 degraded TDAFW pump

Enclosure

7

condition fell within the Special Inspection to Augmented Inspection Team range for

reactive inspections.

2. SPECIAL INSPECl"ION AREAS

2.1 Review of Maintenance

a. Inspection Scope

The team evaluated the adequacy and completeness of the maintenance on the TDAFW

system, including preventive maintenance, procedural guidance, post-maintenance

testing, and supervisory oversight. The team independently evaluated selected

procedures, preventive maintenance strategies. condition reports (CRs). system health

reports. and associated work orders. In addition, the team reviewed the RCA,

conducted equipment walkdowns and interviewed key station personnel. For the

weaknesses identified, the inspectors verified that appropriate corrective actions have

been planned or taken.

b. Findings and Observations

1. Failure to Preclude Recurrence of a Significant Condition Adverse to Quality

Introduction: A self-revealing AV of 10 CFR 50, Appendix S, Criterion XVI, "Corrective

Actions," was identified for the failure to preclude recurrence of a SCAQ associated with

the TDAFW pump governor control valve. Specifically, after identifying corrosion of the

governor control valve stem in April 2005, Ginna did not take adequate corrective

actions to preclude the recurrence of corrosion which led to the binding of the governor

control valve and failure of the TDAFW pump on July 2, 2009. In addition, governor

control valve stem binding was a fikely failure of the May 26, 2009, TDAFW pump

overspeed trip. This finding was preliminarily determined to be White.

Description: On April 11, 2005, Glnna conducted a periodic major inspection of the

TDAFW pump governor control valve under work order #20401907. During the

disassembly of the valve, mechanics noted corrosion in the bushing area of the stem

plug. The vendor recommended replacing the valve stem and plug due to the corrosion.

However, Ginna did not recognize stem corrosion as a condition adverse to quality and

did not initiate a CR in accordance with station guidance in IP-CAP-1 r "Condition

Reporting." As a result, Ginna did not conduct any further analysis or evaluation to

determine the cause of the corrosion. On July 2, 2009, during surveillance testing, the

TDAFW pump tripped due to overspeed. Ginna formed an Issue Response Team and

developed a comprehensive troubleshooting plan to determine the cause(s) of the

failure. The troubleshooting plan consisted of all possible failure modes, possible

causes of each failure mode, and actions to validate or refute each "failure mode. Upon

disassembly of the governor control valve, the stem was found seized within its bushings

and had to be forcibly removed. Visual inspection showed pitting on the surface of the

stem Where it contacted the upper valve bushing. Following completion of the

troubleshooting activities, Ginnaconcluded that TDAFW pump failure was due to binding

of the governor control valve and that the binding was caused by the build up of

corrosion on the valve stem.

Enclosure

8

Governor control valve stem corrosion is an SCAQ because corrosion of the stem can

lead to govemor control valve stem binding and failure of the TDAFW pump as

discussed in NRC IN 94-66: "Overspeed of Turbine-Driven Pumps caused by Governor

Valve Stem Binding," and other related industry operating experience documents.

Immediate corrective actions included entering this condition in the CAP, conducting an

RCA, replacing the governor control valve stem, and conducting weekly monitoring of

the governor control valve during surveillance testing to identify any potential for stem

binding. In addition, corrective actions included a follow-up inspection of the governor

control valve during the fall 2009 refueling outage. Because additional corrosion was

found during this inspection on September 18, 2009, the control valve was sent to the

vendor to be refurbished. Ginna will continue to monitor the governor control valve

under an enhanced TDAFW surveillance program to ensure TDAFW pump operability.

Ginna also was evaluating longer term corrective actions to address the corrosion

including more frequent governor control valve stem replacement, change of the stem

material, and other modifications to the system design. Planned corrective actions

include replacing the stem admission valves in May 2011.

The inspectors noted that governor control valve stem binding also could have been a

contributor to the December 2, 2008, TDAFW pump failure to develop the minimum

acceptable discharge flow and pressure, and the likely cause of the May 26, 2009,

TDAFW pump overspeed trip. Following these events, Ginna missed opportunities to

identify potential stem binding problems after identifying possible indicators of this failure

mode such as leaking steam admission valves and rust/corrosion on the visible portion

of the governor valve stem. In addition, during troubleshooting efforts in May 2009,

. Ginna missed an opportunity to exercise the governor control valve stem with the linkage

disconnected and lube oil pressure not applied. Operating experience suggested that

cycling the valve by hand without hydraulics applied is a prudent action to validate or

refute governor control valve stem binding.

Analysis: The performance deficiency is that Ginna did not take adequate measures to

correct a condition that had the potential to impact the operability of the TDAFW pump.

Specifically, after identifying corrosion on the governor control valve stem in 2005, Ginna

did not take adequate corrective actions to preclude the recurrence of corrosion which

led to the binding of the governor control valve and failure of the TDAFW pump. The

finding is more than minor because it is associated with the equipment performance

attribute of the Mitigating System cornerstone and affects the cornerstone objective to

ensure the availability, reliability, and capability of systems that respond to initiating

events to prevent undesirable consequences. Specifically, stem corrosion caused

binding of the governor control valve and led to the failure of the TDAFW pump.

In accordance with IMe 0609, Attachment 4, "Phase 1 - Initial Screening and

Characterization of Findings," a Phase 2 risk analysis was required because the finding

represents an actual loss of safety function of a single train for greater than the TS

allowed outage time of 7 days. The Phase 2 risk evaluation was performed in

accordance with IMC 0609, Appendix A, Attachment 1, "User Guidance for Phase 2 and

Phase 3 Reactor Inspection Findings for At*,power Situations." Because the precise time

is unknown for the inception of TDAFW pump inoperability, an exposure time of one-half

of the time period (t/2) between discovery (May 26, 2009) to the last successfully

completed quarterly surveHlance test (March 5, 2009) was used. This t/2 exposure time

Enclosure

9

equals 51 days. Using Ginna's Phase 2 SDP notebook, pre-solved worksheets, and an

initiating event likelihood of 1 year (>30-days exposure time), the inspector identified that

this finding is of potentially substantial safety significance (Yellow). The dominant

sequence identified in the Phase 2 notebook involves a loss of offsite power (LOOP),

failure of both EDGs, and the subsequent loss of the TDAFW pump, with the failure of

operators to restore offsite power within 1 hour: LOOP (2) + EAC (3) + TDAFW (0) +

REC1 (0) = 5 (Yellow). In recognition that the Phase 2 notebook typically yields a

conservative result, a NRC Region I Senior Reactor Analyst (SRA) performed a Phase 3

risk assessment of this finding.

The SRA used Ginna's Standardized Plant Analysis Risk (SPAR) model, Revision 3.45,

dated June 2008. and graphical evaluation module, in conjunction with the System

Analysis Programs for Hands-On Integrated Reliability Evaluations (SAPHIRE). Version

7, to estimate the internal risk contribution of the Phase 3 risk assessment. The

following assumptions were used for this assessment:

1. Based on the guidance provided in the Risk Assessment of Operational Events

Handbook, Revision 1.01, the calculated exposure was determined to be 1198

hrs. The summation of this exposeure time was determined as follows:

  • One half the exposure time, (tI2), was applied for the period between

March 5 - May 26, 2009

  • The full exposure time, (t). was applied for the unavailability and

troubleshooting from May 26 - May 29, 2009.

  • One half the exposure time. (tI2), was applied for the period between

June 25 -July 2, 2009

  • The full exposure time, (t), was applied for the unavailability and

troubleshooting from July 2 - July 5, 2009

2. To closely approximate the type of flilure exhibited by the TDAFW pump, the fail

to start basic event <AFW-TDP-FS-TDP> was changed from its baseline failure

probability to 1.0, representing a 100 percent failure to start condition.

3. Based on the nature of the failure. and no recovery procedures in place, there

was no recovery credit assigned to the May failure.

4. The loss of service water initiating event frequency (IE-LOSWS) was increased

from its nominal value of 4.0E-4 to 2.0E*3 to more closely model the risk of a

LOSWS at the Ginna station. This is consistent with Ginna's understanding of

the risk of this event. All remaining events were left at their nominal failure

probabilities.

5, The model was modified by Idaho National Laboratory (INL) to include

convolution correction factors. Convolving the failure distribution eliminates the

simplifying assumption that all failure to run events happen at time=O. Inclusion

of this correction can reduce station blackout (SBO) core damage frequency

(CDF) significantly for plants like Ginna that have low EDG redundancy.

6. Since all observed failures happened upon the initiation of the TDAFW system,

the period between May 29 and June 25 2009, was not included in the exposure

period because the system successfully completed increased, weekly,

surveillance testing. The team could not conclude that the stem binding

condition would occur after the pump had been successfully started and run.

7. Cutset probability calculation truncation was set at 1E-13.

Enclosure

10

Based upon the above assumptions, the Ginna SPAR model calculated an increase in

internal event contribution to conditional core damage probability (CCDP) of 2.9E-6. This

low-ta-mid E-6 delta CCDP value represents a low to moderate safety significance

(White). The dominant internal event sequence involved a LOOP with subsequent

failure of the EDGs (station blackout event), the failure of the TDAFW train and the

failure to recover AC power. The Phase 3 SPAR model results correlate well to the

Phase 2 SDP Notebook dominant core damage sequences.

External Events Risk Contribution

The Ginna Probablistic Safety Assessment (PSA) includes a Level 1 analysis of fires

and flooding external events. The PSA summarizes the fire contribution as representing

approximately 48% of the total (internal and external) core damage frequency, or nearly

half of the annualized risk. The NRC does not have an external event risk model for

Ginna. Consequently, the SRA, after review of the licensee's Individual Plant

Examination of External Events (IPEEE), utilized the licensee's external events

assessment to quantify the fire and flooding events risk contribution for this condition.

Seismic event likelihood was considered to be very low and determined not to be a

significant contributor to the risk of this condition.

The results of the PSA for this condition calculated a CCDP contribution from fire events

at 5E-6 and from flooding at 7E-7. The most significant fire initiated core damage

sequence involved a spectrum of control room fires, with a failure of automatic and

manual suppression, a failure of the TDAFW pump and a failure of the 'C' standby

auxiliary feed water pump for decay heat removal via the steam generators. The most

Significant flooding core damage sequence quantified in the PSA for this condition,

Involved flooding in the relay room, failure of the TDAFW pump and a failure to align

standby auxiliary feed water pump for decay heat removal via the steam generators.

Large Early Release Frequency (LERF) Evaluation

The SRA used IMC 0609, Appendix H, "Containment Integrity Significance

Determination Process," to determine if this finding was a significant contributor to a

large early release. The Ginna containment is classified as a pressurized water reactor

large-dry containment deSign. Based upon the dominant sequences involving LOOP

and station blackout (S80) initiating events, per Appendix H, Table 5.2, "Phase 2

Assessment Factors - Type A Findings at Full Power," the failure of the TDAFW pump

does not represent a significant challenge to containment integrity early in the postUlated

core damage sequences. Consequently, this finding does not screen as a significant

large early release contributor because the close-in populations can be effectively

evacuated far in advance of any postulated release due to core damage, Accordingly,

the risk significance of this finding is associated with the delta CDF value, per IMC 0609,

Appendix H, Figure 5.1, and not delta LERF.

Risk Assessment Summary

The calculated total risk significance of this finding is based upon the summation of

internal and external risk contributions (delta CCDP internal + delta CCDP external (fires

and floods).= delta CCDP total). 2.9E-6 + 5E-6 + 7E-7 = 8.6E-6 delta ceDP.

Enclosure

11

Annualized, this value of 8.6E-6 delta CDF represents a low to moderate safety

significance or White finding.

Licensee's Risk Assessment Summary

Constellation's risk assessment for the given condition, assuming no operator recovery,

resulted in a total delta CDF value of 1.028E-5. This increase in CDF value comprised

of: 4.6E-6 due to intemal events; 0.7E-6 due to intemal flooding events; and 5E-6

fire/external events. Similar to the NRC internal risk contribution, the largest percentage

of intemal risk was derived from station blackout events. The licensee conducted

refinements in their modeling to credit additional recovery options in the event that the

TDAFW pump failed. By crediting these recovery actions, the delta CDF was reduced

from 1.028E-5 to 9.2 E-6, or by approximately 10%. The specific recovery actions are

as follows: .

1. The potential for operators to use standby auxiliary feedwater (SAFW) pump C,

in lieu of the TDAFW pump during fire and flood scenarios which require use of

alternate shutdown procedures was modeled. Although use of an SAFW pump

is not specifically called out in these procedures, the procedures do explicitly

recognize that if the TDAFW pump is not functioning, a loss of secondary heat

sink will result, and direct operators to refer to other emergency procedures for

alternate methods of establishing a heat sink (see ER-FIRE.1 step 4.3.4.2, ER

FIRE.2 step 4.3.12, etc.}. In response to this hypothetical scenario, an

operations Shift Manager (SM) indicated that upon a failure of the TDAFW to

provide flow, a SAFW pump could be manually started by locally opening the

service water suction valve to the pump and locally closing the breaker to the

pump motor. The steps necessary to align an SAFW pump to the steam

generators (SG) are contained in emergency operating procedures (EOP)

Attachment 5.1 'Attachment SAFW'. Since only Busses 14 and 18 are energized

during ER-FIRE scenarios, SAFW pump C would be used.

2. Following the May 26th overspeed trip of the TDAFW pump, new section 2.2

was added to procedure P-15.6, 'Operation of the TDAFW Pump Trip Throttle

Valve.' Revision 00200. This step provides instructions for a 'slow start' of the

TDAFW pump manually, following an overspeed trip of the pump, by using the

trip throttle valve. This allows for starting of the pump even if the governor control

valve is stuck in the full open position following the overspeed trip. This

procedure step was successfully used following both the May 26th failure and

the July 2nd failure. Per Operations management, the shift managers, who

would be directing use of this procedure, were briefed on the updated procedure

to ensure they were aware that new step was available for use and understood

how it was to be performed. A controlled copy of the procedure is located at the

TDAFW pump for use by the operator. Since this procedure was in effect prior

to the July failure exposure period (Le., prior to the last successful TDAFW pump

test on June 25, 2009), it is considered as a recovery for failures of the TDAFW

pump.

Recovery actions identified in #1 above were not quantified by the team however the

evaluation approach appears to be appropriate. Prior to the licensee crediting recovery

actions identified in #2 above, the team was able to verify that the procedures were in

Enclosure

12

place and observed troubleshooting video in which the licensee started the TDAFW

pump with this method. As a result the SRA concluded that the licensee's modeling

demonstrating a risk reduction was appropriate.

Based upon the close comparison between NRC and Constellation risk estimates, no

sensitivity analyses were warranted. The use of V2 to approximate the exposure time

was determined to be appropriate for standby or periodically operated components that

fail due to a degradation mechanism that gradually affects the component during the

standby time period. Inclusion of the unavailability time hours, due to troubleshooting

and repairs, is also appropriate and consistent with the guidance promulgated in Risk

Assessment of Operational Events Handbook, Revision 1.01, dated January 2008.

This finding has a cross-cutting aspect in the area of Problem Identification and

Resolution, Corrective Action Program, because Ginna did not implement a corrective

action program with a low threshold for identifying issues completely, accurately, and in

a timely manner commensurate with their safety significance. Specifically, Ginna did not

identify issues associated with corrosion of the governor control valve within the

corrective actions program. The inspectors concluded that the performance deficiency is

reflective of current performance because Ginna had reasonable opportunities to identify

the issue during troubleshooting in December 2008 and May 2009. P.1(a) per IMC

0305]

Enforcement: 10 CFR 50, Appendix B, Criterion XVI, "Corrective Actions," states, in

part, "Measures shall be established to assure that conditions adverse to quality, such

as failures, malfunctions, defiCiencies, deviations, defective material and eqUipment, and

nonconformances are promptly identified and corrected. In the case of significant

conditions adverse to quality, the measures shall assure that the cause of the condition

is determined and corrective action taken to preclude repetition." Contrary to the above,

after identifying corrosion on the TDAFW pump governor control valve stem on April 11,

2005, which is a significant condition adverse to quality, Ginna did not take adequate

measures to determine the cause and prevent recurrence. The cause of the condition

was left uncorrected and resulted in additional stem corrosion that led to binding of the

governor control valve and the failure of the TDAFW pump on July 2, 2009. In addition,

stem corrosion was the likely cause of the TDAFW pump failure on May 26, 2009. This

issue was entered into Ginna's CAP as CR-:2009-003680 and CR-2009-004577.

Pending final determination of significance, this finding is identified as an AV. (AV

0500024412009008*01: Inadequate Corrective Actions Associated with the TDAFW

Pump Governor Control Valve)

2. Untimely Corrective Actions Associated with Steam Admission Valves

Introduction: A self-revealing NeVof 10 CFR 50, Appendix B, Criterion XVI, "Corrective

Actions," was identified for the failure to establish adequate measures to correct a

longstanding issue associated with steam a(]mission valves leakage. As a result, the

leakage most likely contributed to the build-up of corrosion on the TDAFW pump

governor control valve stem on May 26, 2009 and contributed to the failure of the

TDAFW pump on July 2, 2009.

Description: During a review of failures associated with the TDAFW pump, the

inspectors noted that the steam admission valves had a history of leaking. Based on a

review of the RCA report, industry operating experience, and associated CRs, the

Enclosure

13

inspectors determined that the steam admission valve leakage was a contributing factor

in the development of corrosion of the governor control valve and contributed to the

failure of the TDAFW pump on July 2, 2009, and most likely the failure of the TDAFW

pump overspeed trip failure on May 26, 2009. Based on a review of eRs and interviews

of personnel, the inspectors determined that the steam admission valves had been

leaking since at least 2005.

In July 2005, CR-2005~3660 documented that steam admission valve 3505A was

leaking past its seat. However, Ginna did not take or plan any corrective actions

associated with the issue. By October 2006, steam admission valve 3505A leakage had

increased such that the TDAFW pump turbine was rotating approximately 100 rpm.

Ginna cycled the valve to reduce seat leakage, generated a work order to repair the

valve in May 2008, and conducted an evaluation of past operability. Ginna concluded

that there was no potential for increased consequences with time if the condition

continued. During the May 2008 refueling outage, Ginna conducted a repair of steam

admission valve 3505A. However, this corrective action was not effective; by September

2008, the valve was leaking again although at a reduced rate. The inspectors

determined that Ginna did not recognize or consider the potential impact of the steam

admission valve leakage on the governor control valve stem.

Immediate corrective actions included entering this condition in the CAP, replacing the

govemor control valve stem, and conducting weekly monitOring of the governor control

valve during surveillance te~ting to identify any potential for stem binding. Additionally,

the steam admission valves were inspected and re-worked and the govemor control

valve was Inspected during the fall 2009 outage. Ginna will continue to monitor the

governor control valve under an enhanced TDAFW surveillance program to ensure

TDAFW pump operability. Planned corrective actions include replacing the stem

admission valves in May 2011.

Analysis: The performance deficiency is that Ginna did not adequately address

deficiencies associated with steam admission valve leakage in that the leakage likely

resulted in accelerated corrosion of the governor control valve and contributed to the

failure of the TDAFW pump. The finding is more than minor because it is associated

with the equipment performance attribute of the Mitigating Systems cornerstone and

affects the cornerstone objective to ensure the availability and reliability of systems that

respond to initiating events to prevent undesirable consequences. Specifically, leakage

through the steam admission valves can res.ult in continuous wetting of the governor

control valve stem and lead to or accelerate corrosion of the governor control valve.

This could result in a stem binding of the govemor control valve and failure of the

TDAFW pump. The inspectors evaluated the significance of this finding using IMC 0609,

Attachment 4, "Phase 1 -Initial Screening and Characterization of Findings." The

finding is of very low safety significance because it is not a design or qualification

deficiency, did not represent a loss of a safety function of a system or a single train

greater than its TS allowed outage time, and did not screen as potentially risk Significant

due to external events. The inspectors determined that the steam admission valve

leakage was not a direct cause of the failure of the TDAFW pump overspeed events.

The steam admission valve leakage was a contributing factor in the development of

governor control valve stem corrosion and contributed to the failure of the TDAFW

pump.

Enclosure

14

This finding has a cross-cutting aspect in the area of Problem Identification and

Resolution, Corrective Action Program, because Ginna did not thoroughly evaluate

problems such that the resolutions address causes and extent of conditions, as

r:eecessary, in a timely manner, commensurate with their significance. Specifically,

Ginna did not thoroughly evaluate the potential effect of the steam admission valve

leakage on the governor control valve performance. The inspectors determined that this

issue is reflective of current licensee performance because each time the issue was

identified and a CR was generated represented an opportunity for Ginna to adequately

evaluate the issue and assign appropriate corrective actions. [P.1 (c) per IMC 0305]

Enforcement: 10 CFR Part 50, Appendix B, Criterion XVI, "Corrective Actions," states, in

part. "Measures shall be established to assure that conditions adverse to quality, such

as failures, malfunctions, deficiencies, deviations, defective material and equipment, and

nonconformances are promptly identified and corrected." Contrary to this requirement,

from at least July 2005 to July 2, 2009, Ginna did not established adequate measures to

correct longstanding steam admission valves leakage and/or minimize the impact of the

leakage on the TDAFW pump governor control valve performance. As a result, leakage I*

I

through the steam admission valves contributed to the corrosion of the governor control

valve and contributed to the failure of the TDAFW pump on July 2, 2009 and most likely

the failure of the TDAFW pump on May 26, 2009. Because this violation is of very low

safety significance (Green) and Ginna entered this issue into their CAP for resolution as

CR-2009-003680 and CR-2009-004577, this violation is being treated as an NCV

consistent with the NRC Enforcement Policy. (NCV 0500024412009008-02: Inadequate

Corrective Actions Associated with Stearn Admission Valve Leakage)

2.2 Review of Operating Experience

a. Inspection ScoQe

The team reviewed operating experience involving TDAFW pump failures and actions

taken by the Ginna staff to identify and address these types of failures. In addition, the

team examined the specific issues associated with governor control valve stem binding

to assess any new generic issues of industry interest for prompt communication and

dissemination. As part of this evaluation, the inspectors reviewed pertinent industry

operating experience, Ginna's response to NRC Information Notices, and interviewed

key plant personnel.

b. Findings and Observations

No Findings of Significance Identified.

The inspectors determined that there were no new generic issues identified as a result of

this event. However, the inspectors noted that Ginna missed opportunities to utilize

industry operating experience to identify precursors associated with this event and to

conduct effective troubleshooting. Specifically, following the discovery of corrosion on

the exposed portion of the TDAFW pump govemor control valve stem in May 2005,

Ginna did not enter this issue in to their CAP. As a result Ginna missed an opportunity

to revisit operating experience from NRC IN 94-66 conceming governor control valve

stem binding. In several examples in NRC IN 94-66, sites that experienced governor

control valves stem binding identified stem corrosion following valve disassembly. Ginna

Enclosure

15

had originally determined that NRC IN 94-66 was not applicable to Ginna because the

governor control valve was of a different configuration and material as those discussed

in the IN and that corrosion of the stem had not been previously identified. Although this

may have been a reasonable assessment during the original review of the NRC IN 94-66

in 1994, the inspectors determined that once corrosion of the stem was identified in'May

2005, Ginna missed an opportunity to revisit this operating experience. In addition, as

discussed in Section 2.1.2 of this report. Ginna did not utilize Industry operating

experience in evaluating a condition associated with steam admission valve leakage.

NRC IN 94-66, other industry operating experience, and the vendor technical manual

stated that steam admission valve leakage is a cause related to governor control valve

stem binding. However, Ginna did not consider the impact of steam admission valve

leakage on the governor control valve performance. Finally, the inspectors noted that

Ginna missed opportunities to incorporate industry operating experience during

troubleshooting efforts during the May 2009 TDAFW pump failure. NRC IN 94-66

discussed several examples where a freedom of motion test was performed to test for

stem binding with the governor control valve linkage disconnected and hydraulics not

applied. However, during the May 2009 event, Ginna missed an opportunity to conduct

this test and consequently, missed an opportunity to potentially identify the failure mode

prior to the July 2, 2009, overspeed trip. Ginna captured these issues in their CAP

under CR-2009-003680 and CR-2009-004577..

2.3 Review of Root Cause and Extent-ot-Condition

a. Inspection Scope

The team evaluated the adequacy of Ginna's RCA and completed interim corrective

actions. In addition the team evaluated the adequacy of Ginna's initial extent of

condition for the TDAFW pump failures. The team reviewed plant drawings, procedures,

and associated system modifications. In addition, the team conducted a walkdown of

the TDAFW system and interviewed key Ginna personnel.

b. Findings and Observations

Introduction: The inspectors identified an NCV of 10 CFR 50, Appendix B, Criterion III,

"Design Control," for the failure to establish measures to ensure that a modification

performed on the governor control valve bushing was a suitable application of materials

for the TDAFW pump.

Description: During the troubleshooting and repair of the TDAFW pump in July 2009,

Ginna incorrectly evaluated that a vendor service bulletin allowed for larger stem-to

bushing clearance than was prescribed in their current technical documents. Since

there was overlap between the station technical information and the vendor service

bulletin, Ginna decided to increase the clearance, by lapping the bushings, to reduce the

likelihood that corrosion products would cause the stem to bind. To increase the

clearance, Ginna removed some of the hardened layer on the bushing. During a review

of the RCA, the inspectors determined that Ginna did not consider the potential impact of

removing some ot the hardened layer on the corrosion rate of the governor control valve.

The inspectors noted that by removing some of the hardened layer, the material property

of the bushing could have been changed and/or additional micro-cracks could have been

created or exposed that could increase the corrosion rate or potentially cause other

Enclosure

16

problems such as stem-to~bushing galling. The inspectors noted that if the corrosion

rate is greater than predicted, then planned corrective actions may not be adequate to

maintain the TDAFW pump operable. Additionally, the team was concerned, that by

increasing the stem to bushing clearances, the stem would be susceptible to larger

steam exposure and that this could further accelerate the corrosion. Following concerns

raised by the inspectors, Ginna initiated CR-2009-005959 to ensure that all possible

consequences of lapping the TDAFW pump control valve bushing were fully evaluated.

In addition, Ginna assigned corrective actions to inspect the control valve bushing during

the fall 2009 refueling outage. During performance of the refueling inspection under WO

C90623685, pitting of the stem and corrosion of the bushings were observed.

Constellation initiated CR~2009-006765 and noted that the corrosion of the bushings

appeared to have been caused by the lapping of the bushing to achieve the desired

clearance between the stem and the bushings. The development of corrosion on the

bushing reduced the margin that was predicted to ensure adequate stem movement.

Immediate corrective actions following the inspection of the governor control valve

during the fall 2009 refueling outage included entering this condition in the CAP and

refurbishing the governor control valve with a new stem and bushing.

Analysis: The performance deficiency is that Ginna failed to establish measures to

ensure that a modification performed on the governor control valve bushing was a

suitable application of materials for the TDAFW pump. The finding is more than minor

because it is associated with the equipment performance attribute of the Mitigating

Systems cornerstone and affects the cornerstone objective to ensure the availability and

reliability of systems that respond to initiating events to prevent undesirable

consequences. Specifically, lapping of the valve bushing resulted in an unanticipated

corrosion mechanism of the governor control valve that impacted the reliability of the

TDAFW pump. The inspectors evaluated the Significance of this finding using IMC 0609,

Attachment 4, "Phase 1 -Initial Screening and Characterization of Findings." The

finding is of very low safety significance because it is not a design or qualification

deficiency, did not represent a loss of a safety fUnction of a system or a single train

greater than its TS allowed outage time, and did not screen as potentially risk significant

due to external events.

The inspectors determined that this finding has a cross-cutting aspect in the area of

Human Performance, Decision Making, because Ginna did not make a safety-significant

or risk-significant decision using a systematic process, especially when faced with

uncertain or unexpected plant conditions, to ensure safety was maintained. Specifically,

Ginna did not use a systematic process such as an engineering evaluation to properly

evaluate the potential impact of removing some of the hardened layer of the bushing.

H.1(a) per IMC 0305]

Enforcement: 10 CFR 50, Appendix B, Criterion III, "Design Control" states, in part,

"Measures shall also be established for the selection and review for suitability of

application of materials, parts, equipment, and processes that are essential to the safety

related functions of the structures, systems and components." Contrary to the

requirements, in July 2009, Ginna failed to establish measures to ensure that a

modification performed on the governor control valve bushing was a suitable application

of materials for the TDAFW pump. Specifically, lapping of the valve bushing resulted in

an unanticipated corrosion mechanism of the governor control valve that had the

Enclosure

17

potential to impact the performance of the TDAFW pump if not corrected. Because this

violation is of very low safety significance (Green) and Ginna entered this issue into their

CAP for resolution as CR-2009-006765, this violation is being treated as an NCV

consistent with the NRC Enforcement Policy. (NeV 05000244/2009008-03: Failure To

Establish Design Control Measures Associated With The Turbine Driven Auxiliary

Feedwater Pump Governor Control Valve)

2.4 Risk Assessment of the As-Found Condition

a. Insoection Scope

Prior to the initiation of the Special Inspection Team, the Region I SRA performed a

CCDP assessment which conservatively bounded the potential risk significance of the

degraded condition, assuming the TDAFW pump would fail to star on demand to

mitigate the consequences of an event. The initial CCDP estimate was performed in

accordance with IMC 0309, "Reactive Inspection Decision Basis for Reactors." The SRA

used the Ginna SPAR model and associated GEM to evaluate the potential risk

significance of this condition. The results of the IMC 0309 assessment are documented

in report section 2.1.b.1 above.

b. Final Risk Estimate

Following team review and independent verification of the degraded turbine driven

auxiliary feed water pump governor control valve, the team concluded that for

approximately 119B hours, the TDAFW pump would not have been capable of

responding to an event. Consistent with IMC 0609 conditional core damage probability

assessment methodology, this degraded condition resulted in a loss of operability or

safety function, and therefore was of low to moderate (B.6E-6) safety significance.

4. OTHER ACTIVITIeS

40A6 Meetings, Including Exit

On August 27 and on October 7,2009 the team presented the inspection results to Mr.

John Carlin and other members of the R. E. Ginna Nuclear Power Plant staff. The

inspectors verified that none of the materiall~xamined during the inspection is

considered proprietary in nature.

Enclosure

A-1

ATTACHMENT A

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee personnel

J. Carlin, Site Vice President

E. Larson, Plant General Manager

D. Crowley, Senior Engineer

E. Durkish, Associate Engineer

R. Everett, Supervisor, Primary Systems Engineering

T. Harding, Director, Licensing

R. Ruby, Principal Engineer, Licensing

P. Swift, Engineering Manager

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

05000244/2009008-01 AV Failure to Preclude Recurrence of a

Significant Condition Adverse to Quality

Associated with the Turbine Driven Auxiliary

Feedwater Pump Governor Control Valve.

(Section 2.1.1)

Opened/Closed

05000244/2009008-02 NCV Inadequate Corrective Actions Associated

with Steam Admission Valve Leakage.

(Section 2.1.2)05000244/2009008-03 NCV Failure to Establish Design Control

Measures Associated with the Turbine

Driven Auxiliary Feedwater Pump Governor

Control Valve. (Section 2.3)

I.IST OF DOCUMENTS REVIEWED

In addition to the documents identified in the body of this report, the inspectors reviewed the

following documents and records:

Corrective Actions

CA-2009-002311

Condition Reports

CR-2003-2006 CR-2005-3660 CR-2006-006029 CR-2006-006341

CR-2005-1509 CR-2005-5513 CR-2006-006204 CR-2006-006962

Attachment A

A-2

CR-2007-000876 CR-2008-009911 CR-2009-004590 CR-2009-005959*

CR-2007-001302 CR-2009-003680 CR-2009-004591 CR-2009-006765*

CR-2008-003687 CR-2009-004222* CR-2009-005964

CR-2008-007541 CR-2009-004577

  • NRC Identified During Inspection

Corrective Action Tracking System

CATS R007325

Procedures

AP-FVV.1, Abnormal MFW Pump Flow or NPSH, Revision 01702

PT-16QT-T, Auxiliary Feedwater Turbine Pump - Quarterly, Revision 05900

CNG-MN-1.01-1002, Troubleshooting, Revision 0001

CNG-CA-1.01, Corrective Action Program, Revision 0001

CNG-CA-1.01-1004, Root Cause Analysis, Revision 0001

CNG-CA-1.01-1005, Apparent Cause Evaluation, Revision 0100

CNG-CA-1.01-1006, Common Cause Analysis, Revision 0001

CNG-CA-1.01-1007, Trending, Revision 0000

CNG-CA-1.01-1010, Use of OE, Revision 0000

IP-CAP-1, Ginna Condition Reporting, Revision 02800

M-11.5C, Auxiliary Feedwater Pump Motor Mechanical Inspection and Maintenance,

Revision 03000

0-1.1, Plant Heatup From Cold Shutdown to Hot Shutdown, Revision 16301

PT-16Q-T, Auxiliary Feedwater Turbine Pump - Quarterly, Revision 05600. Completed

3/14/08,514108,5/5/08,6/11/08,9/4/08, 1213/08, 1214/08, 12111/08, 12/18/08,2/12/09,

5/26/09, 5/28/09

Surveillance Tests

PT-16Q-T, Auxiliary Feedwater Turbine Pump - Quarterly, Revision 05600, 03/14/2008

PT-16Q-T, Auxiliary Feedwater Turbine Pump -. Quarterly, Revision 05700, 05/04/2008

PT-16Q-T, Auxiliary Feedwater Turbine Pump _. Quarterly, Revision 05700,05/05/2008

PT-16Q-T, Auxiliary Feedwater Turbine Pump - Quarterly, Revision 05700. 06/11/2008

STP-0-16-COMP-T, Auxiliary Feedwater Turbine Pump - Comprehensive Test,

Revision 00000, 06/11/2008

PT-16Q-T, Auxiliary Feedwater Turbine Pump - Quarterly. Revision 05701, 09/03/2008

PT-16Q-T, Auxiliary Feedwater Turbine Pump - Quarterly, Revision 05701, 12/02/2008

PT-16Q-T, Auxiliary FeedwaterTurbine Pump - Quarterly. Revision 05701,12103/2008

PT-16Q-T. Auxiliary Feedwater Turbine Pump _. Quarterly, Revision 05701, 12/04/2008

PT-16Q-T, Auxiliary Feedwater Turbine Pump _. Quarterly, Revision 05702, 12/11/2008

PT-16Q-T, Auxiliary Feedwater Turbine Pump _. Quarterly, Revision 05702, 12/18/2008

PT-16Q-T, Auxiliary Feedwater Turbine Pump - Quarterly, Revision 05801, 01116/2009

PT-16Q-T, AUXiliary Feedwater Turbine Pump - Quarterly, Revision 05801, 02112/2009

PT-16Q-T, AUXiliary Feedwater Turbine Pump _. Quarterly. Revision 05900,05/26/2009

PT-16Q-T, Auxiliary Feedwater Turbine Pump - Quarterly, Revision 05900,05/28/2009

STP-0-16-COMP-T, Auxiliary Feedwater Turbine Pump - Comprehensive Test,

Revision 00400, 05/28/2009

Attachment A

A-3

Work Orders

W020604989

W020401907

Drawings

DWG No. 33013-1231, Main Steam System, Revision 37

DWG No. 33013-2285, Motor Driven and Turbine Driven Auxiliary Feedwater Pumps

Lube Oil Skid, Revision 17

DWG No. LB-112541, Turbine Control and Quick Start System

DWG No. T040-001A, TDAFW Control Oil System, Revision 0

DWG No. T040-002A, TDAFW Turbine Trip Valve, Revision 0

DWG No. T040-003A, Auxiliary and Standby Aux. Feedwater Systems, Revision 2

DWG No. T040-003B, SAFW System 1-Line Diagram, Revision 0

DWG No. T040-003C, AFW System 1-Une Diagram, Revision 1

DWG No. T040-004A, Auxiliary Feedwater Pump Auto Start Signals, Revision 0

DWG No. T830-004A, Blowdown Isolation Solenoid Control Circuit, Revision 0

Other Documents

Vendor Report, Preliminary Results ofStem Sticking Failure Mechanisms, July 20, 2009

Vendor Report 09-1929 Part 1, Equipment Root Cause Analysis of AFWP Control Valve

Stem Sticking Problem at Ginna Nuclear Power Station

Vendor Technical Question Response, August 26, 2009

Category I Root Causal Analysis, May and July 2009 Turbine Driven Auxiliary Feedwater

Pump (TDAFWP) Failures; Overspeed Trip During Testing

vrD-E9016-4001, Excerpts from EPRI Manual 1007461, Terry Turbine Maintenance

Guide, AFW Application, Revision 000

vrD-G0153-4001, Operating Instructions Easy Flow Body Combined Trip Throttle Valve,

Revision 2

VrD-W0315-4001, Instructions For 465 H.P. Non-Condensing Steam Turbine Serial

Number 26635, Revision 000

VrD-W0315-4002, Service Department Standards Book No. 10, Field Service Manual,

Revision 000

Response to NRC Generic Letter 90-3, Relaxation of Staff Position In Generic Letter 83

28, Item 2.2 Part 2 "Vendor Interface for Safety Related Components, dated

September 18, 1990

CATS 10 R04451, Response to NRC IN 94-66, OVERSPEED OF TURBINE-DRIVEN

PUMPS CAUSED BY GOVERNOR VALVE STEM BINDING

CMM-37-19-9519E, Worthington Turbine Driven Auxiliary Feedwater Pump Hydraulic

Governor Control Valve Maintenance for 9519E, Revision 00200

Constellation Energy Nuclear Generating Group Reply to a Notice of Violation; EA-09

045

Engineering Change Package No. ECP-2009-0146, TDAFW Lube Oil Orifice

Management Review Committee Agenda. August 5, 2009

Purchase Requisition No. 58686, Dresser-Rand Valve Stem

Technical Staff Request 97-199, Leakoff from TDAFW Govenor Valve 9519E

Management Review Committee Agenda, August 5, 2009

Purchase Requisition No. 58686, Dresser-Rand Valve Stem

Attachment A

A-4

Technical Staff Request 97-199, Leakofffrom TDAFW Govenor Valve 9519E

Turbine Driven Auxiliary Feedwater Pump Preventive Maintenance Strategies

Auxiliary Feed Water System, 1st Quarter 200S

Auxiliary Feed Water System. 2nd Quarter 200S

Auxiliary Feed Water System. 3rd Quarter 200S

Auxiliary Feed Water System, 4th Quarter 200S

Auxiliary Feed Water System, 1st Quarter 2009

Operating Experience

OE-200S-000397

OE-200S-000607

OE-200S-000847

oE-20OS-00S60

OE-2008-001296

OE-2009-00212

OE*2009*001178

Oil Analysis

Pump IB Oil Analysis. 2008-03

Pump OB Oil Analysis, 2008-03

Reservoir Oil Analysis 2008-05

Reservoir Oil Analysis 2008-08

Reservoir Oil Analysis 2009-05

Attachment A

A-4

LIST OF ACRONYMS

AV Apparent Violation

CAP Corrective Action Program

CCDP Conditional Core Damage Probability

CDF Core Damage Frequency

CR Condition Report

DRP Division of Reactor Projects

EDG Emergency Diesel Generator

GEM Graphical Evaluation Module

ICCDP Incremental Conditional Core Damage Probability

IMC Inspection Manual Chapter

IN Information Notice

INL Idaho National Labs

  • IPEEE Individual Plant Examination of External Events

LERF Large Early Release Frequency

LOOP Loss of Offsite Power

LOSWS Loss of Service Water System

NCV Non Cited Violation

NRC Nuclear Regulatory Commission

NRR Office of Nuclear Reactor Regulation

PARS Publicly Available Records

PSA Probabilistic Safety Assessment

RCA Root Cause Analysis

SAFW Standby Auxiliary Feedwater

SBO Station Blackout

SOP Significance Determination Process

SPAR Standardized Plant Analysis Risk

SRA Senior Reactor Analyst

SCAQ Significant Condition Adverse to Quality

NCV Non-citied Violation

TBD To Be Determined

TDAFW Turbine Driven Auxiliary Feedwater

TS Technical Specification

Attachment A

8-1

Special Inspection Charter

R.E. Ginna Nuclear Power Plant

Failure of the Turbine-Driven Auxiliary Feedwater (TDAFW) Pump

on May 26, 2009 and July 2, 2009

Background:

On May 26, 2009, during routine quarterly surveillance testing of the turbine driven

auxiliary feedwater (TDAFW) system, the TDAFW pump tripped on overspeed. The test

was repeated several hours later and the TDAFW pump tripped again on overspeed.

Fluctuations in oil pressure were observed during the testing.

After extensive troubleshooting, Ginna personnE~1 identified a number of issues but no

definitive cause for the overspeed trips. The lube/control oil system was drained and

cleaned due to the presence of fine particulates; a pressure pulsation dampener

accumulator bladder was replaced due to a below normal pressure condition; the oil

pressure regulating bypass valve was replaced due to potential cycling; a change to

linkage setup was implemented; governor relay valve, and trip and throttle valve parts

were replaced due to out of specification clearances; and a miSSing oil line orifice was

installed. Following these corrective actions, the system was successfully tested and

declared operable.

Constellation is completing a root cause evaluation and the resident inspectors continue

to conduct baseline inspections with assistance from DRS specialists. Testing of the

TDAFW system will be at an increased frequency until Constellation has confidence that

the system is performing as required.

On July 2, 2009, during the performance of the increased frequency surveillance, the

TDAFW pump again tripped on overspeed. Glnna personnel discovered pitting and

corrosion on the stem of the governor control valve during troubleshooting activities to

restore the pump to operable status. This Special Inspection Team had raised concerns

regarding corrosion on the stem of the Governor Control Valve during onsite inspection

activities the week of June 15, 2009.

Basis for the Formation of the SIT:

The failure of the TDAFW pump involved repetitive failures of this safety~related

eqUipment. There have been three failures of the TDAFW pump since December 2008.

On December 2, 2008, a failure was attributed to inadequate implementation of the

preventive maintenance program. SpeCifically, the governor linkages were not

lubricated in March 2008 which resulted in the pump's inability to achieve the required

flow and pressure in December 2008. On July 2, 2009, the failure was preliminarily

determined to be caused by pitting on the stem of the Governor Control valve and overly

tolerances causing binding of the stem. Although the specific failure modes (overspeed

trip, inability to achieve the required flow or pressure) were different, the underlying

cause of inadequate or inappropriate preventive maintenance may be the same.

Attachment 8

B-2

Based upon best available information, the Region I Senior Reactor Analyst (SRA)

conducted a preliminary risk estimate of the May 26 TDAFW pump failure. An

incremental conditional core damage probability (ICCDP) in the upper E-6 range (8E-6

per the 82 day exposure period), was calculated using the Ginna SPAR model.

assuming that the TDAFW pump would not have started since the last time it passed a

surveillance test on March 5 until May 26 (82 days). The dominant core damage

sequence was a station blackout (LOOP with failure of both EDGs,) with no TDAFW and

failure to recover offsite power or an EDG in one hour.

Based upon the preliminary conditional core damage probability estimate of upper E-6

range, in accordance with IMC 0309, this event falls within the region for a Special

Inspection Team.

Oblectives of the Special Inspection:

The objectives of the special inspection are to review and assess: (1) Constellation's

planning and execution of the risk significant work activities on the TDAFW system; (2)

equipment issues related to the TDAFW testing; and (3) Constellation's response to this

significant equipment failure.

To accomplish these objectives, the following will be performed:

1. Evaluate the adequacy and completeness of the maintenance on the TDAFW

system, including preventive maintenance, procedural guidance, post

maintenance testing, and supervisory oversight.

2. Evaluate Constellation's application of pertinent industry operating experience

and evaluation of potential precursors, including the effectiveness of any actions

taken in response to the operating experience or precursors.

3. Evaluate the adequacy of Constellation's response to the TDAFW system

failures, including Constellation's cause analysis and completed interim corrective

actions.

4. Evaluate the adequacy of Constellation's initial extent of condition for the TDAFW

failures, as appropriate.

5. Evaluate the failure modes for potential generic implications including the need

for generic communications

Additionally, the team leader will review lessons learned from the Special Inspection

and, if appropriate, prepare a feedback form on recommendations for revising the

reactor oversight process (ROP) baseline inspection procedures in order to proactively

identify the issues and causes involved with the event.

Guidance:

Inspection Procedure 93812, "Special Inspection", provides additional guidance to be

used by the Special Inspection Team. Team duties will be as described in Inspection

Procedure 93812. The inspection should emphasize fact-finding in its review of the

circumstances surrounding the event. It is not the responsibility of the team to examine

Attachment B

8-3

the regulatory process. Safety concerns identified that are not directly related to the

event should be reported to the Region I office for appropriate action.

The Team will conduct an entrance meeting and begin the inspection on June 8,2009.

While on site, the Team Leader wi" provide daily briefings to Region I management, who

will coordinate with the Office of Nuclear Reactor Regulation, to ensure that all other

parties are kept informed. A report documenting the results of the inspection should be

issued within 45 days of the completion of the inspection.

This Charter may be modified should the team develop significant new information that

warrants review.

Attachment 8