IR 05000244/2022002

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LLC - Integrated Inspection Report 05000244/2022002
ML22214A180
Person / Time
Site: Ginna Constellation icon.png
Issue date: 08/03/2022
From: Erin Carfang
Division of Operating Reactors
To: Rhoades D
Constellation Energy Generation, Constellation Nuclear
References
IR 2022002
Download: ML22214A180 (13)


Text

August 3, 2022

SUBJECT:

R.E. GINNA NUCLEAR POWER PLANT, LLC - INTEGRATED INSPECTION REPORT 05000244/2022002

Dear David Rhoades:

On June 30, 2022, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at R.E. Ginna Nuclear Power Plant, LLC. On July 14, 2022, the NRC inspectors discussed the results of this inspection with Daren Blankenship, Site Vice President, and other members of your staff. The results of this inspection are documented in the enclosed report.

No findings or violations of more than minor significance were identified during this inspection.

This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely, Erin E. Carfang, Chief Projects Branch 1 Division of Operating Reactor Safety Docket No. 05000244 License No. DPR-18

Enclosure:

As stated

Inspection Report

Docket Number:

05000244

License Number:

DPR-18

Report Number:

05000244/2022002

Enterprise Identifier: I-2022-002-0033

Licensee:

Constellation Energy Generation, LLC

Facility:

R.E. Ginna Nuclear Power Plant, LLC

Location:

Ontario, New York

Inspection Dates:

April 1, 2022 to June 30, 2022

Inspectors:

J. Schussler, Senior Resident Inspector

C. Dukehart, Acting Resident Inspector

C. Swisher, Resident Inspector

S. Haney, Senior Project Engineer

S. Veunephachan, Health Physicist

Approved By:

Erin E. Carfang, Chief

Projects Branch 1

Division of Operating Reactor Safety

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at R.E. Ginna Nuclear Power Plant, LLC, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

No findings or violations of more than minor significance were identified.

Additional Tracking Items

None.

PLANT STATUS

Ginna began the inspection period operating at rated thermal power and remained at, or near, rated thermal power for the inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures in effect at the beginning of the inspection unless otherwise noted. Currently approved inspection procedures with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html.

Samples were declared complete when the inspection procedure requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed activities described in Inspection Manual Chapter 2515, appendix D, Plant Status, conducted routine reviews using IP 71152, Problem Identification and Resolution, observed risk significant activities, and completed on-site portions of inspection procedures. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

Seasonal Extreme Weather Sample (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated readiness for seasonal extreme weather conditions prior to the onset of high temperatures and heat advisories of the following systems on June 17, 2022:
  • Charging pump room
  • Battery rooms
  • Relay room

Impending Severe Weather Sample (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated the adequacy of the overall preparations to protect risk significant systems from impending severe weather due to a tornado watch issued for Wayne and Monroe Counties on June 16, 2022

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (5 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1)

'B' emergency diesel generator while 'A' emergency diesel generator was out-of-service for planned maintenance on April 19, 2022 (2)

'C' safety injection following the completion of a quarterly surveillance test on May 17, 2022

(3) Turbine driven auxiliary feedwater following the completion of a quarterly surveillance test on May 26, 2022 (4)

'A' train of spent fuel pool cooling while in service on June 13, 2022 (5)

'A' residual heat removal following the completion of a quarterly surveillance test on June 16, 2022

71111.05 - Fire Protection

Fire Area Walkdown and Inspection Sample (IP Section 03.01) (5 Samples)

The inspectors evaluated the implementation of the fire protection program by conducting a walkdown and performing a review to verify program compliance, equipment functionality, material condition, and operational readiness of the following fire areas:

(1) Standby auxiliary feedwater annex on April 7, 2022 (2)

'A' emergency diesel generator cable vault on April 19, 2022

(3) Relay room on May 6, 2022
(4) Technical Support Center and associated diesel and ventilation rooms on May 13, 2022
(5) Residual heat removal subbasement on May 20, 2022

Fire Brigade Drill Performance Sample (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated the on-site fire brigade training and performance during an unannounced fire drill on June 2, 2022

71111.06 - Flood Protection Measures

Inspection Activities - Internal Flooding (IP Section 03.01) (1 Sample)

The inspectors evaluated internal flooding mitigation protections in the:

(1) Flood exclusion zone and barrier wall in the screen house operating floor during major disassembly/reassembly of 'B' traveling screen on May 19, 2022

71111.07A - Heat Exchanger/Sink Performance

Annual Review (IP Section 03.01) (1 Sample)

The inspectors evaluated readiness and performance of:

(1) 'A' component cooling water heat exchanger on June 30, 2022

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)

(1) The inspectors observed and evaluated licensed operator performance in the control room during:
  • Shift turnover from day shift to night shift on April 27, 2022
  • Containment depressurization and performance of the planned electric plant configuration change from two offsite circuits to one on May 9, 2022
  • Turbine driven auxiliary feedwater surveillance test and the resulting licensed operator reactivity management on May 24, 2022

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

(1) The inspectors observed and evaluated licensed operator performance in the simulator during licensed operator requalification training on May 31, 2022. The training involved a scenario that contained, but was not limited to, atmospheric relief valve failure, turbine control valve failure and a steam generator tube leak.

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (6 Samples)

The inspectors evaluated the accuracy and completeness of risk assessments for the following planned and emergent work activities to ensure configuration changes and appropriate work controls were addressed:

(1) Evaluation of plant risk (action green) during planned 'A' emergency diesel generator engine, relays, and fuel oil system maintenance on April 13, 2022
(2) Evaluation of plant risk (action green) during planned 'C' standby auxiliary feedwater flow switch replacement, transmitter flow calibration, and motor operated valve maintenance on April 27, 2022
(3) Elevated plant risk (green) during planned maintenance of offsite circuit 7T components including transformer 7 work in switchyard 13A, transformer 12A in switchyard 13, associated circuit breakers on May 10, 2022
(4) Elevated plant risk (green) during planned maintenance, efficiency testing and charcoal sample testing on the 'B' control room emergency air treatment system on May 25, 2022
(5) Elevated plant risk (green) during planned maintenance, cleaning, and inspection of the 'B' component cooling water heat exchanger on May 25, 2022
(6) Elevated plant risk (green) and corresponding system availability during turbine driven auxiliary feedwater comprehensive test on June 14, 2022

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 03.01) (7 Samples)

The inspectors evaluated the licensee's justifications and actions associated with the following operability determinations and functionality assessments:

(1)

'A' emergency diesel generator operability evaluation following elevated lube oil temperature when the lube oil temperature switch was not properly controlling the lube oil heaters on April 25, 2022

(2) Safety injection system operability evaluation when the pump minimum recirculation flow path was not in the normal standby configuration on June 9, 2022 (3)

'A' emergency diesel generator operability evaluation following fuel oil leaks from the fuel injection pump dogbone fittings on cylinder 1R and 7L and a leak from the fuel header connection at cylinder 1L on June 13, 2022

(4) Reactor coolant system loop operability evaluation following degraded 'A' reactor coolant pump seal leak off flow rate on June 21, 2022
(5) Reactor coolant pressurizer level instrumentation reactor trip circuitry operability evaluation following channel deviation on June 30, 2022 (6)

'B' auxiliary feedwater pump lube oil motor operability evaluation during increased motor inboard vertical vibration reading on June 30, 2022

(7) Offsite circuit functional assessment when circuit 7T transfer trip lockout relay light extinguished on June 30, 2022

71111.19 - Post-Maintenance Testing

Post-Maintenance Test Sample (IP Section 03.01) (5 Samples)

The inspectors evaluated the following post-maintenance testing activities to verify system operability and/or functionality:

(1) Operational testing of the diesel driven air compressor following planned maintenance including an oil change, filter replacement, air filter replacement and inspections of the coolant and air compressor fluid on April 14, 2022
(2) Operational testing of the 'A' emergency diesel generator and fuel oil system following planned maintenance of the protective relays, air system, fuel oil system and engine maintenance on April 20, 2022
(3) System operation to correctly control diesel lube oil temperature in specified range following unplanned maintenance to remove a new style 'A' emergency diesel generator lube oil temperature switch and replace it with the previous existing style on April 27, 2022
(4) Operational testing of the 'C' standby auxiliary feedwater system following planned replacement of the discharge flow switch, flow transmitter calibration and motor operated valve lubrication on April 28, 2022
(5) Operational testing of the 'B' diesel driven FLEX air compressor following planned maintenance including an oil change, filter replacement, air filter replacement and inspections of the coolant and air compressor fluid on June 17, 2022

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance testing activities to verify system operability and/or functionality:

Surveillance Tests (other) (IP Section 03.01) (3 Samples)

(1) STP-O-2.2QA, "Residual Heat Removal Pump A In-service Test" on May 20, 2022
(2) STP-E-10.1, "Station Battery B Quarterly Inspection" on May 23, 2022
(3) STP-O-16-COMPT-T, "Auxiliary Feedwater Turbine Pump Comprehensive Test" on May 25, 2022

In-service Testing (IP Section 03.01) (1 Sample)

(1) STP-O-2.1-COMP-C, "Safety Injection Pump C Comprehensive Test" on May 17, 2022

71114.06 - Drill Evaluation

Drill/Training Evolution Observation (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated an emergency drill in the simulator control room and emergency offsite facility involving an Alert, Site Area Emergency and General Emergency declaration due to a scenario which contained, but was not limited to, a simulated loss of coolant accident in a reactor coolant loop, fuel failure and auxiliary building penetration failure on June 7,

RADIATION SAFETY

71124.08 - Radioactive Solid Waste Processing & Radioactive Material Handling, Storage, &

Transportation

Radioactive Material Storage (IP Section 03.01)

The inspectors evaluated the licensees performance in controlling, labeling, and securing the following radioactive materials:

(1) Radioactive materials containers in storage outside in a temporary yard area and within the upper radwaste storage building
(2) Part 37 radioactive materials and selected sealed sources

Radioactive Waste System Walkdown (IP Section 03.02) (2 Samples)

The inspectors walked down the following accessible portions of the solid radioactive waste systems and evaluated system configuration and functionality:

(1) Solid radioactive waste system
(2) Radioactive liquid processing systems

Waste Characterization and Classification (IP Section 03.03) (2 Samples)

The inspectors evaluated the following characterization and classification of radioactive waste:

(1) Resin shipment number 2021-046. U.S. Department of Transportation
Description:

UN3321, Radioactive Material 7, LSA II, RQ, Fissile excepted. Waste Class A Unstable

(2) Dry active waste shipment number 2021-019. U.S. Department of Transportation
Description:

UN3321, Radioactive Material 7, LSA II, Fissile excepted. Waste Class A Unstable

Shipping Records (IP Section 03.05) (4 Samples)

The inspectors evaluated the following non-excepted radioactive material shipments through a record review:

(1) Shipment number 2021-046, UN3321, LSA II, Class AU resin waste
(2) Shipment number 2021-084, UN3321, LSA II, Class AU dry active waste
(3) Shipment number 2021-091, UN3321, LSA II, Class AU dry active waste
(4) Shipment number 2021-095, UN3321, LSA II, Class AU dry active waste

OTHER ACTIVITIES - BASELINE

===71151 - Performance Indicator Verification

The inspectors verified licensee performance indicators submittals listed below:

MS05: Safety System Functional Failures Sample (IP Section 02.04)===

(1) Submitted data from April 1, 2021 through March 31, 2022

BI01: Reactor Coolant System Specific Activity Sample (IP Section 02.10) (1 Sample)

(1) Submitted data from April 1, 2021 through March 31, 2022

BI02: Reactor Coolant System Leak Rate Sample (IP Section 02.11) (1 Sample)

(1) Submitted data from April 1, 2021 through March 31, 2022

===71152S - Semi-annual Trend Problem Identification and Resolution

Semi-annual Trend Review (Section 03.02)===

(1) The inspectors reviewed the licensees corrective action program for potential emerging or adverse trends that might be indicative of a more significant safety issue.

INSPECTION RESULTS

Assessment: Corrective Action Program Semi-annual Trend Review 71152S The inspectors reviewed Constellations corrective action program and evaluated a sample of issues and events that occurred from January 2022 through June 2022 at Ginna. The inspectors then verified whether the issues were appropriately evaluated by Constellation for emerging or adverse trends and addressed within the scope of the corrective action program or through department review.

The inspection did not reveal any new trends that could indicate a more significant safety issue. The inspectors determined that Constellation personnel were identifying trend issues at a low threshold and entered them into the corrective action program for resolution. The inspectors noted low level or precursor trends identified by Constellation relating to the following: RM-14A radiation monitor, offsite circuit manhole float switches, configuration control, human performance precursors, and cold weather issues. The inspectors noted several issue reports relating to emergency light failures. The inspectors discussed the circumstances of the failures with Constellation staff and verified actions were in place to correct the deficiencies. As a result, the inspectors determined station emergency light deficiencies were being entered and trended in the corrective action program.

Based on the overall results of the semi-annual trend review, the inspectors determined that Constellation had properly identified adverse trends at Ginna before they became more significant safety problems. The inspectors independently evaluated the deficiencies noted above for significance in accordance with the guidance in Inspection Manual Chapter 0612, Appendix B, Issue Screening, and Appendix E, Examples of Minor Issues. The inspectors determined that none of the conditions were deficiencies of greater than minor significance and, therefore, are not subject to enforcement action in accordance with the NRCs Enforcement Policy.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On May 12, 2022, the inspectors presented the 71124.08 Debrief inspection results to Paul Swift, Site Vice President, and other members of the licensee staff.
  • On July 14, 2022, the inspectors presented the integrated inspection results to Daren Blankenship, Site Vice President, and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.04

Corrective Action

Documents

Resulting from

Inspection

04506184

Small Boric Acid Leak Around End Plug on Flange Leading

to FI-672

06/17/2022

04506187

Dry Boric Acid on 712B RHR Hx Bypass Valve

06/17/2022

04506193

Dry Boric Acid on 712A RHR Hx Bypass Isolation Valve

06/17/2022

04506198

Dry NaOH Leak Residue on 873B Valve

06/17/2022

71111.05

Corrective Action

Documents

Resulting from

Inspection

04495968

Small Roof Leak Behind Bus 14

04/27/2022

71111.06

Corrective Action

Documents

Resulting from

Inspection

04499326

Dry Water Stains Identified Below DCPDPCD05B

05/12/2022

71111.13

Corrective Action

Documents

Resulting from

Inspection

04501864

Clarification Desired in Functional Restoration Attachment

05/25/2022

71111.15

Corrective Action

Documents

04464494

Increasing Vibration Trend on MIV for PLO12B (AFWP B LO

PMP)

2/03/2021

04470459

Pzr Level Channels Deviation Rising

01/07/2022

04479321

Circuit 7T Transfer Trip Lockout Relay Light Extinguished

2/19/2022

04494484

Minor Leak on Dogbone Fitting of KDG01A Cylinders 1R &

7L

04/20/2022

04494486

Minor Leak from Fuel Header Connection at EDG A Cylinder

1L

04/20/2022

04494996

TS-2882 A DG LO Temp Switch Controlling High

04/22/2022

04496618

Momentary Drop on RCP A #1 Seal Leakoff

04/29/2022

04500140

Valves Found Out-of-position During STP-O-2.1-COMP-C

05/16/2022

Miscellaneous

ACMP OP-AA-108-111 Pressurizer Level Deviation

Revision 0

71111.22

Corrective Action

Documents

Resulting from

04500269

AB-18 AB BSMT EAST EMERG LIGHT Lamp Found

Directed Wrong Direction

05/17/2022

04500287

Dry Inactive Boric Acid Downstream 898J SI Pump Suction C 05/17/2022

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Inspection

Disch Vent

04501144

Dry Boric Acid Leak on V-650F (SFP Leak Drain Hose

Connection)

05/21/2022

04501145

Dry Boric Acid on Flange Downstream of V-2784

05/21/2022

04501146

Dry Boric Acid Leak V-782 Low Suction Isolation Valve TP

SFP (ALT)

05/21/2022

71124.08

Procedures

RP-AA-500-

10003

CFR Part 37 Material Accountability Program

Revision 5

RW-AA-100

Process Control Program for Radioactive Wastes

Revision 12

Radiation

Surveys

URWSB Weekly Survey

04/30/2022

DI Vault Upper/Lower Survey

04/13/2022

Waste Hold Up Tank Room Survey

04/15/2022

Drumming Station

04/06/2022

Shipping Records RP-20210909-

00001

Shipment Number: 2021-046 Resin

09/09/2021

RP-20211118-

00003

Shipment Number: 2021-84 DAW and Metal Scrap

10/11/2021

RP-20211118-

00010

Shipment Number: 2021-091 DAW and Metal Scrap

11/18/2021

RP-20211118-

00017

Shipment Number: 2021-095 DAW Metal Scrap

11/18/2021

71152S

Corrective Action

Documents

04472486

Trending IR for Cold Weather Issues

01/18/2022

04478343

Operations Trend IR - Configuration Control Precursors

2/15/2022

04483684

Trending IR for Offsite Manholes Float Switches

03/09/2022

04493342

Training Potential Trend - HU Learning Opportunities

04/15/2022

04497617

Potential Trend IR: RM-14A Failed Source Checks

05/04/2022