IR 05000244/2019004

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R.E Ginna Nuclear Power Plant, LLC: Integrated Inspection Report 05000244/2019004
ML20037A118
Person / Time
Site: Ginna Constellation icon.png
Issue date: 02/05/2020
From: Erin Carfang
Division Reactor Projects I
To: Bryan Hanson
Exelon Generation Co, Exelon Nuclear
References
IR 2019004
Download: ML20037A118 (15)


Text

February 5, 2020

SUBJECT:

R.E. GINNA NUCLEAR POWER PLANT, LLC - INTEGRATED INSPECTION REPORT 05000244/2019004

Dear Mr. Hanson:

On December 31, 2019, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at R.E. Ginna Nuclear Power Plant, LLC. On January 28, 2020, the NRC inspectors discussed the results of this inspection with Mr. Daren Blankenship, Plant Manager and other members of your staff. The results of this inspection are documented in the enclosed report.

The NRC inspectors did not identify any finding or violation of more than minor significance during this inspection.

This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Erin E. Carfang, Chief Reactor Projects Branch 1 Division of Reactor Projects

Docket No. 05000244 License No. DPR-18

Enclosure:

As stated

Inspection Report

Docket Number:

05000244

License Number:

DPR-18

Report Number:

05000244/2019004

Enterprise Identifier: I-2019-004-0034

Licensee:

Exelon Generation Company, LLC

Facility:

R.E. Ginna Nuclear Power Plant, LLC

Location:

Ontario, NY

Inspection Dates:

October 01, 2019 to December 31, 2019

Inspectors:

J. Schussler, Senior Resident Inspector

M. Montecalvo, Acting Resident Inspector

H. Anagnostopoulos, Senior Health Physicist

E. Andrews, Health Physicist

P. Cataldo, Senior Resident Inspector

E. Dipaolo, Senior Reactor Inspector

P. Ott, Operations Engineer

S. Shaffer, Senior Health Physicist

Approved By:

Erin E. Carfang, Chief

Reactor Projects Branch 1

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at R.E. Ginna Nuclear Power Plant, LLC, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

No findings or violations of more than minor significance were identified.

Additional Tracking Items

None.

PLANT STATUS

Ginna began the inspection period at 100 percent power. The unit remained at, or near, 100 percent power for the entire inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed plant status activities described in IMC 2515, Appendix D, Plant Status, and conducted routine reviews using IP 71152, Problem Identification and Resolution. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

Seasonal Extreme Weather Sample (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated readiness for seasonal extreme weather conditions on December 18, 2019

71111.04Q - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (2 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1)

'A' emergency diesel generator system during 'B' emergency diesel generator 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> surveillance test run on October 28, 2019 (2)

'A' auxiliary feedwater following 'B' auxiliary feedwater surveillance test on November 26, 2019

71111.04S - Equipment Alignment

Complete Walkdown Sample (IP Section 03.02) (1 Sample)

(1)

'A' spent fuel pool cooling, following 'A' spent fuel pool pump testing on November 19, 2019

71111.05Q - Fire Protection

Quarterly Inspection (IP Section 03.01) (4 Samples)

The inspectors evaluated fire protection program implementation in the following selected areas:

(1)

'B' battery room on October 2 and 3, 2019

(2) Relay room on November 17, 2019
(3) Air handling room on December 15, 2019
(4) Turbine building basement on December 15, 2019

71111.07A - Heat Sink Performance

Annual Review (IP Section 02.01) (1 Sample)

The inspectors evaluated readiness and performance of:

(1) 'A' emergency diesel generator lube oil and jacket water heat exchangers on December 13, 2019

71111.11A - Licensed Operator Requalification Program and Licensed Operator Performance

Requalification Examination Results (IP Section 03.03) (1 Sample)

(1) The inspectors reviewed and evaluated the licensed operator examination failure rates for the requalification annual operating exam completed on November 22, 2019

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)

(1) The inspectors observed and evaluated licensed operator performance in the main control room during a planned load reduction in preparation for a scheduled turbine driven auxiliary feedwater pump surveillance test on October 10, 2019 and a scheduled 'B' emergency diesel generator 24-hour surveillance test on October 28, 2019.

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

(1) The inspectors observed and evaluated licensed operator performance in the simulator during licensed operator examinations on November 13, 2019. The examination involved a scenario that contained, but was not limited to, a loss off all offsite power circuits, pressurizer pressure transmitter failure, component cooling water pump failing to run, main steam isolation valves failing to isolate, safety injection trains failing to actuate, and a residual heat removal pump failing to start.

71111.12 - Maintenance Effectiveness

Routine Maintenance Effectiveness Inspection (IP Section 02.01) (1 Sample)

The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions:

(1) Main steam system (System 81) on December 4, 2019

Quality Control (IP Section 02.02) (1 Sample)

The inspectors evaluated maintenance and quality control activities associated with the following equipment performance activities:

(1) Commercial grade dedication and receipt inspection of an emergency diesel generator fitting, electrical diode, half inch relief valve, and an orifice plate on December 17, 2019

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated the risk assessments for the following planned and emergent work activities:

(1) Planned maintenance, elevated risk (yellow), flow calibration of AOV-111, on October 18, 2019
(2) Planned maintenance, elevated risk (green), 7T offsite power circuit system outage window, on October 21, 2019
(3) Planned maintenance, elevated risk (yellow), alternate reactor cooling system injection pump out of service on November 4, 2019
(4) Planned maintenance, elevated risk (yellow), 'A' emergency diesel generator system outage window on November 13, 2019

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 02.02) (6 Samples)

The inspectors evaluated the following operability determinations and functionality assessments:

(1) Pressure relief tank transmitter spikes on November 1, 2019 (2)

'B' battery room water intrusion on November 7, 2019 (3)

'A' motor driven auxiliary feedwater coupling elevated vibrations on November 8, 2019 (4)

'A' and 'B' emergency diesel generator common cause fuel fitting failure on November 8, 2019

(5) Turbine driven auxiliary feedwater, hand controller HVC-487B failure on November 18, 2019
(6) Emergency diesel generator transfer pump elevated vibrations, re-baseline pump on December 16, 2019

71111.18 - Plant Modifications

Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02) (3 Samples)

The inspectors evaluated the following temporary or permanent modifications:

(1)

'A' reactor vessel level indication system temporary modification, ECP-19-000414 on November 20, 2019 (2)

'B' battery room modification, water intrusion, ECP-19-000559 on December 2, 2019 (3)

'A' and 'B' emergency diesel generator sump modification, ECP-19-000479 on December 16, 2019

71111.19 - Post-Maintenance Testing

Post-Maintenance Test Sample (IP Section 03.01) (6 Samples)

The inspectors evaluated the following post maintenance tests:

(1) Service water flow to 'B' motor driven auxiliary feedwater pump lube oil cooler unplanned corrective maintenance and follow up of deficiencies on October 4, 2019
(2) Turbine driven auxiliary feedwater main control board hand controller HCV-487B replacement, unplanned maintenance on October 9, 2019
(3) Service water AOV-4651 valve stroke time testing following planned maintenance on October 11, 2019
(4) Alternate reactor coolant system injection portable pump following planned maintenance on October 22, 2019 (5)

'B' Service water pump comprehensive surveillance test following planned maintenance on November 5, 2019 (6)

'A' emergency diesel generator system outage window on November 15, 2019

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance tests:

Surveillance Tests (other) (IP Section 03.01)

(1) STP-O-16QA, 'A' motor driven auxiliary feedwater on October 9, 2019
(2) STP-O-16QT, turbine driven auxiliary feedwater on October 11, 2019
(3) STP-O-12.2-24, 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> 'B' emergency diesel generator run on October 31, 2019
(4) STP-O-36QD, 'D' standby auxiliary feedwater on November 1, 2019

FLEX Testing (IP Section 03.02) (1 Sample)

(1) STP-O-40.4, standby auxiliary feedwater diesel generator run test (30 percent load) and STP-O-40.10, alternate reactor cooling system injection pump flow test on November 6, 2019

71114.06 - Drill Evaluation

Drill/Training Evolution Observation (IP Section 03.02) (1 Sample)

The inspectors evaluated:

(1) The inspectors evaluated a simulator drill involving an Unusual Event and Alert declaration due to a loss of both offsite circuits and main steam isolation valves failing to close coincident with a steam line break in the plant on November 7,

RADIATION SAFETY

71124.06 - Radioactive Gaseous and Liquid Effluent Treatment

Walk Downs and Observations (IP Section 02.01) (1 Sample)

(1) The inspectors walked down the gaseous and liquid radioactive effluent monitoring and filtered ventilation systems to assess the material condition and verify proper alignment according to plant design.

Calibration and Testing Program (Process & Effluent Monitors) (IP Section 02.02) (1 Sample)

(1) The inspectors evaluated the gaseous and liquid effluent monitor instrument calibration and testing.

Sampling and Analysis (IP Section 02.03) (1 Sample)

(1) The inspectors reviewed:

1. Radioactive effluent sampling activities

2. Representative sampling requirements

3. Compensatory measures taken during effluent discharges with inoperable

effluent radiation monitoring instrumentation

4. The use of compensatory radioactive effluent sampling

5. The results of the inter-laboratory and intra-laboratory comparison program,

including scaling of hard-to-detect isotopes

Instrumentation and Equipment (IP Section 02.04) (1 Sample)

(1) The inspectors reviewed radioactive effluent discharge system surveillance test results and reviewed the methodology used to determine the radioactive effluent stack and vent flow rates based on Technical Specifications/Off Site Dose Calculation Manual acceptance criteria.

Dose Calculations (IP Section 02.05) (1 Sample)

(1) The inspectors reviewed several liquid and gaseous discharge permits to evaluate public dose calculations (monthly, quarterly, and annual) and the annual radiological effluent release reports for 2017 and

OTHER ACTIVITIES - BASELINE

===71151 - Performance Indicator Verification

The inspectors verified licensee performance indicators submittals listed below:

OR01: Occupational Exposure Control Effectiveness Sample (IP Section 02.15)===

(1) The inspectors reviewed licensee submittals for the occupational radiological occurrences PI for the fourth quarter 2018 through the third quarter of 2019.

PR01: Radiological Effluent Technical Specifications/Offsite Dose Calculation Manual Radiological Effluent Occurrences (RETS/ODCM) Radiological Effluent Occurrences Sample (IP Section 02.16) (1 Sample)

(1) The inspectors reviewed licensee submittals for the radiological effluent TS/ODCM radiological effluent occurrence PI for the fourth quarter 2018 through the third quarter of 2019.

71152 - Problem Identification and Resolution

Semiannual Trend Review (IP Section 02.02) (1 Sample)

(1) The inspectors reviewed the licensees corrective action program for potential adverse trends that might be indicative of a more significant safety issue on December 19, 2019.

Annual Follow-up of Selected Issues (IP Section 02.03) (1 Sample)

The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:

(1) A main steam isolation valve failed to close as expected by main control room switch or pushbutton, Action Request

INSPECTION RESULTS

Observation: A Main Steam Isolation Valve Failed to Close as Expected by Main Control Room Switch or Pushbutton 71152 The inspectors performed an in-depth review of Exelons actions following the failure of the A Main Steam Isolation Valve (MSIV) to close following attempts using the Main Control Room hand switch (1/3517) and pushbutton (PB/LAFA) during a plant shutdown on June 16, 2019. A third attempt to close the valve using the hand switch successfully closed the valve. The inspectors reviewed the cause analysis, troubleshooting records, the corrective actions taken and planned, and the extent of condition. The inspectors assessed Exelons problem identification threshold, causal analysis, prioritization and timeliness of corrective actions to determine whether Exelon had taken timely and appropriate corrective actions.

The inspectors observed that Exelons work group evaluation for the issue provided a detailed evaluation of the event and thorough review of the associated equipment issues. The cause of the failure was determined to be a mechanically bound and galled hand switch, 1/3517, that prevented makeup of the switch contacts on the first attempt. The second, more forceful attempt successfully closed the MSIV. The failure to close the valve using the pushbutton (PB/LAFA) was determined to be due to the MSIVs air-operated valve open solenoids being energized. This was because the mechanically bound hand switch inadvertently traveled to the open position and engaged the MSIV open contacts when the operator manually returned the switch to the Auto position following the first attempt to close the MSIV. The inspectors verified that Exelon properly evaluated the issue, performed a thorough review of operating experience, and performed or planned appropriate corrective actions.

Observation: Semi-Annual Trend Review 71152 The inspectors reviewed Exelons corrective action program (CAP) for trends that might be indicative of a more significant safety issue on December 19, 2019. The inspectors evaluated a sample of issues and events that occurred over the course of the third and fourth quarters of 2019 to determine whether issues were appropriately considered as emerging or adverse trends. The inspectors verified that these issues were addressed within the scope of the CAP or through department review.

The evaluation did not reveal any new trends that could indicate a more significant safety issue. The inspectors determined that Exelon personnel were identifying trend issues at a low threshold, entered them into the CAP for resolution and had appropriately prioritized investigation reviews. The inspectors noted minor adverse trends identified by Exelon staff in the areas of the frequency of non-reportable spills, less than adequate use of human performance tools by workers, less than adequate preventative maintenance reviews in engineering, and increased frequency of spurious main control board alarms on the vital battery monitoring system.

Based on the overall results of the semi-annual trend review, the inspectors determined that Exelon had properly identified adverse trends at Ginna before they became more significant safety problems. The inspectors independently evaluated the deficiencies noted above for significance in accordance with the guidance in IMC 0612, Appendix B, Issue Screening, and Appendix E, Examples of Minor Issues. The inspectors determined that none of the conditions were deficiencies of greater than minor significance and, therefore, are not subject to enforcement action in accordance with the NRCs Enforcement Policy.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On October 4, 2019, the inspectors presented the radioactive gaseous and liquid effluent treatment inspection results to E. John Fischer and other members of the licensee staff.
  • On November 21, 2019, the inspectors presented the 'A' main steam isolation valve failed to close as expected by main control room switch or pushbutton inspection results to E. John Fischer and other members of the licensee staff.
  • On January 28, 2020, the inspectors presented the integrated inspection results to Mr. Daren Blankenship, Plant Manager, and other members of the licensee staff.

THIRD PARTY REVIEWS

Inspectors reviewed the Institute on Nuclear Power Operations report that were issued during the inspection period.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.04Q Corrective Action

Documents

Resulting from

Inspection

04300096

71111.05Q Corrective Action

Documents

Resulting from

Inspection

284753

Procedures

STP-O-13.4.33

Station Halon System Bottle Weighing and S08 (Relay

Room and Computer Room) Air Flow Test

Revision 006

71111.12

Corrective Action

Documents

4068566

4190080

207454

21143

Corrective Action

Documents

Resulting from

Inspection

284419

04301459

Miscellaneous

Main Steam (System 81) Maintenance Rule System Basis

Document

19-09

Maintenance Rule Expert Panel Meeting

07/15/2019

19-10

Maintenance Rule Expert Panel Meeting Minutes

07/22/2019

71111.15

Corrective Action

Documents

281616

282792

Corrective Action

Documents

Resulting from

Inspection

286955

Engineering

Evaluations

ECP-16-000669,

Technical

Evaluation

Revision

0000

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

relating to 'B'

Battery Room

ESR-19-0196,

Technical

Evaluation

relating to 'B'

Battery Room

ESR-19-0220, 'A'

EDG common

cause failure

evaluation based

on 'B' EDG

cracked nipple

71111.18

Corrective Action

Documents

263604

71111.22

Corrective Action

Documents

Resulting from

Inspection

286032

286704

71152

Corrective Action

Documents

257220

Corrective Action

Documents

Resulting from

Inspection

04301741

284066

284067

284072

284273

284068

284731

292129

284786

286472

Drawings

10905-0732

Main Steam Isolation Valve A (AOV-3517) Elementary

Wiring Diagram

21946-0732

Main Steam Isolation Valve A (AOV-3517) Control

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Schematic

33013-0663

Safeguard System SI Racks Safety Injection Sequence and

Main Steamline Isolation

Miscellaneous

VTD-W120-4189

Westinghouse Oil-Tite Pushbuttons Flush and Extended

Operators Vendor Technical Manual

Procedures

ER-AA-1200

Critical Component Failure Clock

ER-AA-310-1003

Maintenance Rule-Performance Criteria Selection

PI-AA-120

Issue Identification and Screening Process

PI-AA-125

Corrective Action Program Procedure

Work Orders

C93712470

C93712474