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| | number = ML14163A050 | | | number = ML14163A050 |
| | issue date = 06/13/2014 | | | issue date = 06/13/2014 |
| | title = Summary of Conference Call with Arkansas Nuclear One, Unit 2, Regarding the Spring Steam Generator Inspections (TAC No. MF3897) | | | title = Summary of Conference Call with Arkansas Nuclear One, Unit 2, Regarding the Spring Steam Generator Inspections |
| | author name = Kulesa G J | | | author name = Kulesa G |
| | author affiliation = NRC/NRR/DE/ESGB | | | author affiliation = NRC/NRR/DE/ESGB |
| | addressee name = Markley M T | | | addressee name = Markley M |
| | addressee affiliation = NRC/NRR/DORL/LPLIV | | | addressee affiliation = NRC/NRR/DORL/LPLIV |
| | docket = 05000368 | | | docket = 05000368 |
| | license number = NPF-006 | | | license number = NPF-006 |
| | contact person = Diaz-Colon M D | | | contact person = Diaz-Colon M |
| | case reference number = TAC MF3897 | | | case reference number = TAC MF3897 |
| | document type = Meeting Summary, Memoranda | | | document type = Meeting Summary, Memoranda |
| | page count = 4 | | | page count = 4 |
| | project = TAC:MF3897 | | | project = TAC:MF3897 |
| | stage = | | | stage = Other |
| }} | | }} |
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| =Text= | | =Text= |
| {{#Wiki_filter: June 13, 2014 MEMORANDUM TO: Michael T. Markley, Chief Plant Licensing Branch IV-1 Division of Operating Reactor Licensing Office of Nuclear Reactor Regulation FROM: Gloria J. Kulesa, Chief /RA/ Steam Generator Tube Integrity and Chemical Engineering Branch Division of Engineering Office of Nuclear Reactor Regulation | | {{#Wiki_filter:June 13, 2014 MEMORANDUM TO: Michael T. Markley, Chief Plant Licensing Branch IV-1 Division of Operating Reactor Licensing Office of Nuclear Reactor Regulation FROM: Gloria J. Kulesa, Chief /RA/ |
| | Steam Generator Tube Integrity and Chemical Engineering Branch Division of Engineering Office of Nuclear Reactor Regulation |
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| ==SUBJECT:== | | ==SUBJECT:== |
| SUMMARY OF CONFERENCE CALL WITH ARKANSAS NUCLEAR ONE, UNIT 2, REGARDING THE SPRING 2014 STEAM GENERATOR INSPECTIONS (TAC NO. MF3897)
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| On May 27, 2014, the staff of the Steam Generator Tube Integrity and Chemical Engineering Branch (ESGB) of the Division of Engineering participated in a conference call with representatives of Entergy Nuclear Operations, Inc. (the licensee) regarding the ongoing steam generator (SG) inspection activities at Arkansas Nuclear One, Unit 2. In support of the conference call, the licensee provided the document attached to the enclosed conference call summary. Please include Kenneth J. Karwoski, Andrew B. Johnson, and me on distribution of the final document. Please include me on concurrence only if you have made significant changes to the enclosed summary. Please close this TAC upon issuance of the enclosed summary. ESGB formally reviews all SG inspection summary report(s) submitted by licensees in accordance with the plant's technical specification (TS) requirements. The licensees submit the summary report(s) following the completion of the SG tube inspections at a frequency defined by their TSs. Therefore, please provide the report(s) and a work request to me when submitted.
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| The process for handling our review of SG inspection summary reports, as well as the SG conference calls, is outlined in a March 12, 2009, memo from Michele G. Evans to Joseph G. Giitter (Agencywide Documents Access and Management System Accession Number ML090710575). We appreciate your support in this matter.
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| Docket No. 50-368 | | ==SUMMARY== |
| | OF CONFERENCE CALL WITH ARKANSAS NUCLEAR ONE, UNIT 2, REGARDING THE SPRING 2014 STEAM GENERATOR INSPECTIONS (TAC NO. MF3897) |
| | On May 27, 2014, the staff of the Steam Generator Tube Integrity and Chemical Engineering Branch (ESGB) of the Division of Engineering participated in a conference call with representatives of Entergy Nuclear Operations, Inc. (the licensee) regarding the ongoing steam generator (SG) inspection activities at Arkansas Nuclear One, Unit 2. In support of the conference call, the licensee provided the document attached to the enclosed conference call summary. Please include Kenneth J. Karwoski, Andrew B. Johnson, and me on distribution of the final document. Please include me on concurrence only if you have made significant changes to the enclosed summary. Please close this TAC upon issuance of the enclosed summary. |
| | ESGB formally reviews all SG inspection summary report(s) submitted by licensees in accordance with the plants technical specification (TS) requirements. The licensees submit the summary report(s) following the completion of the SG tube inspections at a frequency defined by their TSs. Therefore, please provide the report(s) and a work request to me when submitted. |
| | The process for handling our review of SG inspection summary reports, as well as the SG conference calls, is outlined in a March 12, 2009, memo from Michele G. Evans to Joseph G. Giitter (Agencywide Documents Access and Management System Accession Number ML090710575). We appreciate your support in this matter. |
| | Docket No. 50-368 |
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| ==Enclosure:== | | ==Enclosure:== |
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| As stated | | As stated CONTACT: Marioly Diaz Colon, NRR/DE 301-415-2849 |
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| CONTACT: Marioly Diaz Colon, NRR/DE 301-415-2849 June 13, 2014 MEMORANDUM TO: Michael T. Markley, Chief Plant Licensing Branch IV-1 Division of Operating Reactor Licensing Office of Nuclear Reactor Regulation FROM: Gloria J. Kulesa, Chief /RA/ Steam Generator Tube Integrity and Chemical Engineering Branch Division of Engineering Office of Nuclear Reactor Regulation
| | June 13, 2014 MEMORANDUM TO: Michael T. Markley, Chief Plant Licensing Branch IV-1 Division of Operating Reactor Licensing Office of Nuclear Reactor Regulation FROM: Gloria J. Kulesa, Chief /RA/ |
| | Steam Generator Tube Integrity and Chemical Engineering Branch Division of Engineering Office of Nuclear Reactor Regulation |
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| ==SUBJECT:== | | ==SUBJECT:== |
| SUMMARY OF CONFERENCE CALL WITH ARKANSAS NUCLEAR ONE, UNIT 2, REGARDING THE SPRING 2014 STEAM GENERATOR INSPECTIONS (TAC NO. MF3897)
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| On May 27, 2014, the staff of the Steam Generator Tube Integrity and Chemical Engineering Branch (ESGB) of the Division of Engineering participated in a conference call with representatives of Entergy Nuclear Operations, Inc. (the licensee) regarding the ongoing steam generator (SG) inspection activities at Arkansas Nuclear One, Unit 2. In support of the conference call, the licensee provided the document attached to the enclosed conference call summary. Please include Kenneth J. Karwoski, Andrew B. Johnson, and me on distribution of the final document. Please include me on concurrence only if you have made significant changes to the enclosed summary. Please close this TAC upon issuance of the enclosed summary. | | ==SUMMARY== |
| | OF CONFERENCE CALL WITH ARKANSAS NUCLEAR ONE, UNIT 2, REGARDING THE SPRING 2014 STEAM GENERATOR INSPECTIONS (TAC NO. MF3897) |
| | On May 27, 2014, the staff of the Steam Generator Tube Integrity and Chemical Engineering Branch (ESGB) of the Division of Engineering participated in a conference call with representatives of Entergy Nuclear Operations, Inc. (the licensee) regarding the ongoing steam generator (SG) inspection activities at Arkansas Nuclear One, Unit 2. In support of the conference call, the licensee provided the document attached to the enclosed conference call summary. Please include Kenneth J. Karwoski, Andrew B. Johnson, and me on distribution of the final document. Please include me on concurrence only if you have made significant changes to the enclosed summary. Please close this TAC upon issuance of the enclosed summary. |
| | ESGB formally reviews all SG inspection summary report(s) submitted by licensees in accordance with the plants technical specification (TS) requirements. The licensees submit the summary report(s) following the completion of the SG tube inspections at a frequency defined by their TSs. Therefore, please provide the report(s) and a work request to me when submitted. |
| | The process for handling our review of SG inspection summary reports, as well as the SG conference calls, is outlined in a March 12, 2009, memo from Michele G. Evans to Joseph G. Giitter (Agencywide Documents Access and Management System Accession Number ML090710575). We appreciate your support in this matter. |
| | Docket No. 50-368 |
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| ESGB formally reviews all SG inspection summary report(s) submitted by licensees in accordance with the plant's technical specification (TS) requirements. The licensees submit the summary report(s) following the completion of the SG tube inspections at a frequency defined by their TSs. Therefore, please provide the report(s) and a work request to me when submitted.
| | ==Enclosure:== |
| The process for handling our review of SG inspection summary reports, as well as the SG conference calls, is outlined in a March 12, 2009, memo from Michele G. Evans to Joseph G. Giitter (Agencywide Documents Access and Management System Accession Number ML090710575). We appreciate your support in this matter. Docket No. 50-368
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| ==Enclosure:==
| | As stated CONTACT: Marioly Diaz Colon, NRR/DE 301-415-2849 DISTRIBUTION: |
| | DE R/F EMurphy AObodoako RidsNrrPMArkansas JDrake ADAMS Accession Number: ML14163A050 OFFICE NRR/DE/ESGB NRR/DE/ESGB NRR/DE NRR/DE/ESGB NAME MDiaz-Colon AJohnson KKarwoski GKulesa DATE 06/ 12 /2014 06/ 12 /2014 06/ 12 /2014 06/ 13 /2014 OFFICIAL RECORD COPY |
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| | CONFERENCE CALL |
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| As stated CONTACT: Marioly Diaz Colon, NRR/DE 301-415-2849
| | ==SUMMARY== |
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| DISTRIBUTION: DE R/F EMurphy AObodoako RidsNrrPMArkansas JDrake ADAMS Accession Number: ML14163A050 OFFICE NRR/DE/ESGB NRR/DE/ESGB NRR/DE NRR/DE/ESGB NAME MDiaz-Colon AJohnson KKarwoski GKulesa DATE 06/ 12 /2014 06/ 12 /2014 06/ 12 /2014 06/ 13 /2014 OFFICIAL RECORD COPY Enclosure CONFERENCE CALL SUMMARY ARKANSAS NUCLEAR ONE, UNIT 2, REGARDING SPRING 2014 STEAM GENERATOR INSPECTIONS DOCKET NO. 50-368 TAC NO. MF3897 On May 27, 2014, the staff of the Steam Generator Tube Integrity and Chemical Engineering Branch (ESGB) of the Division of Engineering participated in a conference call with representatives of Entergy Nuclear Operations, Inc. (the licensee) regarding the ongoing steam generator (SG) inspection activities at Arkansas Nuclear One, Unit 2 (ANO-2). In support of the conference call, the licensee provided the document attached to this conference call summary.
| | ARKANSAS NUCLEAR ONE, UNIT 2, REGARDING SPRING 2014 STEAM GENERATOR INSPECTIONS DOCKET NO. 50-368 TAC NO. MF3897 On May 27, 2014, the staff of the Steam Generator Tube Integrity and Chemical Engineering Branch (ESGB) of the Division of Engineering participated in a conference call with representatives of Entergy Nuclear Operations, Inc. (the licensee) regarding the ongoing steam generator (SG) inspection activities at Arkansas Nuclear One, Unit 2 (ANO-2). In support of the conference call, the licensee provided the document attached to this conference call summary. |
| Additional clarifying information not included in the document provided by the licensee is summarized below. | | Additional clarifying information not included in the document provided by the licensee is summarized below. |
| * ANO-2 replaced the original SGs with Westinghouse Model Delta 109 SGs. The replacement SGs have been in service for 14 calendar years. The fourth SG inservice inspections are being performed in the current refueling outage (refueling outage 23). The SGs are at the end of their first inspection interval defined by the technical specifications. ANO-2 has been inspecting the SGs every third refueling outage. | | * ANO-2 replaced the original SGs with Westinghouse Model Delta 109 SGs. The replacement SGs have been in service for 14 calendar years. The fourth SG inservice inspections are being performed in the current refueling outage (refueling outage 23). The SGs are at the end of their first inspection interval defined by the technical specifications. ANO-2 has been inspecting the SGs every third refueling outage. |
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| * No tube-to-tube wear was identified in the current outage. | | * No tube-to-tube wear was identified in the current outage. |
| * There were a total of 80 AVB indications in both SGs in the previous inspection. | | * There were a total of 80 AVB indications in both SGs in the previous inspection. |
| * The inspections identified no wear associated with loose parts. | | * The inspections identified no wear associated with loose parts. |
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| | Enclosure |
| * The secondary side inspections performed in both SGs did not identify any erosion or cracks in the feed ring, primary or secondary steam separators, or the outlet venturi. | | * The secondary side inspections performed in both SGs did not identify any erosion or cracks in the feed ring, primary or secondary steam separators, or the outlet venturi. |
| * The licensee clarified that the three machine remnants referenced on page 5 refer to very small machine turnings (i.e., lathe turning). | | * The licensee clarified that the three machine remnants referenced on page 5 refer to very small machine turnings (i.e., lathe turning). |
| * An evaluation of blockage of the top support plate will be done as part of the eddy current auto-analysis that is verifying the position of the AVBs. | | * An evaluation of blockage of the top support plate will be done as part of the eddy current auto-analysis that is verifying the position of the AVBs. |
| * At the time of the call, the licensee stated that approximately 100 percent of the eddy current analysis was complete and the AVB location analysis still had two weeks until completion. | | * At the time of the call, the licensee stated that approximately 100 percent of the eddy current analysis was complete and the AVB location analysis still had two weeks until completion. |
| * The licensee confirmed that the replacement SGs did not have a stay cylinder, that the center region formerly occupied by the stay cylinder had been filled in with tubes, and that there was a six-inch wide open lane in the middle of the replacement SGs. The following abbreviations are used in the document provided by the licensee: | | * The licensee confirmed that the replacement SGs did not have a stay cylinder, that the center region formerly occupied by the stay cylinder had been filled in with tubes, and that there was a six-inch wide open lane in the middle of the replacement SGs. |
| 2R22 = Unit 2 Refueling Outage 22 ANO2 = Arkansas Nuclear One, Unit 2 CMOA = Conditional Monitoring Operational assessment CR-ANO-2-2014-01539 = Condition Report EPRI = Electric Power Research Institute ETSS = examination technique specification sheet NEI 97-06 = Nuclear Energy Institute Steam Generator Program Guidelines N/A = not applicable NDE = nondestructive evaluation PWR = pressurized water reactor REV = Revision TTS = Top of tubesheet The staff did not identify any issues that required follow-up action at this time; however, the staff asked to be notified in the event that any unusual conditions were detected during the remainder of the outage. | | The following abbreviations are used in the document provided by the licensee: |
| | | 2R22 = Unit 2 Refueling Outage 22 ANO2 = Arkansas Nuclear One, Unit 2 CMOA = Conditional Monitoring Operational assessment CR-ANO-2-2014-01539 = Condition Report EPRI = Electric Power Research Institute ETSS = examination technique specification sheet NEI 97-06 = Nuclear Energy Institute Steam Generator Program Guidelines N/A = not applicable NDE = nondestructive evaluation PWR = pressurized water reactor REV = Revision TTS = Top of tubesheet The staff did not identify any issues that required follow-up action at this time; however, the staff asked to be notified in the event that any unusual conditions were detected during the remainder of the outage.}} |
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Letter Sequence Other |
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MONTHYEARML14104B6092014-04-17017 April 2014 Discussion Points for Telephone Conference on 5/22/14 for Upcoming Steam Generator Tube Inservice Inspection Project stage: Other ML14163A0502014-06-13013 June 2014 Summary of Conference Call with Arkansas Nuclear One, Unit 2, Regarding the Spring Steam Generator Inspections Project stage: Other ML14170A0602014-06-23023 June 2014 Summary of 5/27/2014 Conference Call Regarding Refueling Outage Steam Generator Inspection Project stage: Other 2014-06-13
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Category:Meeting Summary
MONTHYEARML24017A2982024-04-18018 April 2024 Summary of Regulatory Audit Regarding the License Amendment Request to Revise Technical Specifications to Adopt TSTF 505, Revision 2, Provide Risk-Informed Extended Completion Times RITSTF Initiative 4b ML24052A2572024-02-26026 February 2024 Summary of January 17, 2024, Partially Closed Teleconference Meeting with Entergy Operations, Inc. to Discuss Proposed License Amendment Request for Entergy Fleet Regarding Implementation of an Online Monitoring Methodology ML23257A2412023-09-19019 September 2023 Summary of August 15, 2023, Pre-submittal Teleconference with Entergy Operations, Inc. to Discuss Proposed License Amendment Request Concerning Pressurizer Heaters for Arkansas Nuclear One, Unit 1 ML23047A3822023-03-21021 March 2023 Summary of December 15, 2022 Periodic Advanced Reactor Stakeholder Public Meeting ML22215A1912022-08-0909 August 2022 Summary of July 13, 2022, Teleconference Meeting with Entergy Operations, Inc. to Discuss Planned License Amendment Requests to Adopt Technical Specifications Task Force (TSTF) Traveler 505, Risk-Informed Extended Completion Times ML22147A0932022-06-0606 June 2022 2021 Annual Assessment Public Meeting Summary ML22151A1302022-06-0202 June 2022 May 10, 2022, Summary of Teleconference Meeting W/Entergy Operations, Inc. to Discuss a Planned Alternative for a One-Time Schedule Extension for the In-Service Examination of Control Rod Drive Mechanism Penetration No. 1 in the Reactor Ves ML22125A2452022-05-0909 May 2022 May 3, 2022, Summary of Teleconference Meeting with Entergy Operations, Inc. to Discuss Proposed License Amendment Request for ANO, Units 1 & 2 Regarding Proposed Revision to Emergency Plan and On-Shift Staff Analysis ML22003A0562022-01-10010 January 2022 Summary of December 16, 2021, Presubmittal Teleconference with Entergy Operations, Inc. to Discuss Proposed Amendment Request Concerning TS 3.4.4, RCS Loops, Modes 1 and 2, for Arkansas Nuclear One, Unit 1 ML21323A0472021-12-0606 December 2021 Summary of Public Meeting on November 5, 2021, with the National Organization of Test, Research, and Training Reactors on Operator Licensing for Research and Test Reactors ML21288A0392021-10-18018 October 2021 September 14, 2021, Summary of Public Workshop on Scale/Melcor Source Term Demonstration Project - Pebble-Bed Molten-Salt-Cooled Reactor ML21181A3352021-07-0101 July 2021 June 23, 2021, Summary of Public Meeting to Discuss Technology Inclusive Content of Application Project ML21158A2232021-06-0808 June 2021 Meeting Summary for Ticap Workshop 3 ML21140A3892021-05-24024 May 2021 Riv Column 1 EOC 2020 Public Meeting Summary ML21132A2952021-05-14014 May 2021 Summary of Public Meeting to Discuss Technology Inclusive Content of Application Project ML21117A0262021-05-0505 May 2021 Summary of Teleconference with Entergy Operations, Inc. to Discuss Forthcoming LAR Concerning Reactor Coolant System Primary Activity and Primary-to-Secondary Leak Rate ML20337A1572020-12-0808 December 2020 Summary of Teleconference Meeting with Entergy Operations, Inc. to Discuss the Forthcoming Supplemental Response Concerning Generic Letter 2004-02 for Arkansas Nuclear One, Units 1 and 2 ML20287A4012020-10-26026 October 2020 Summary of September 17, 2020, Meeting with Entergy to Discuss Proposed License Amendment Request for Arkansas Nuclear One, Units 1 and 2 Request to the Extend Allowable Outage Time for the Emergency Cooling Pond ML20260G9992020-09-16016 September 2020 Summary of August 4, 2020, Teleconference Meeting with Entergy Operations, Inc. to Discuss Proposed License Amendment Request for Arkansas Nuclear One, Units 1 and 2 Regarding Adoption of 10 CFR 50.69 ML20189A2832020-07-0707 July 2020 Summary of Region IV Annual Assessment Public Meeting ML20153A2252020-06-0404 June 2020 April 29, 2020, Summary of Meeting with Entergy Operations, Inc. to Discuss a Proposed Relief Request Use of Carbon Fiber Reinforced Polymer Piping for Underground Service Water Piping at Arkansas Nuclear One, Units 1 and 2 ML19182A0332019-07-10010 July 2019 Summary of Teleconference with Entergy Operations, Inc. Regarding Proposed License Amendment Request Revised Fuel Handling Analysis and Adoption of Various TSTF Travelers for Arkansas Nuclear One, Unit 2 ML18176A1312018-06-21021 June 2018 Summary of Annual Assessment Meeting with Entergy Operations, Inc., Regarding 2017 Performance of Arkansas Nuclear One ML18107A4972018-04-27027 April 2018 April 10, 2017, Summary of Public Meeting with Entergy Nuclear Operations, Inc. Regarding Upcoming License Amendment Request to Add Setpoint Verification Requirement to Technical Specification Surveillance Requirements ML18099A0712018-04-16016 April 2018 March 20, 2018, Summary of Meeting with the Nuclear Energy Institute and Other Industry Representatives Regarding the Surveillance Frequency Control Program ML17353A1542017-12-22022 December 2017 Summary of Public Meeting with Entergy Operations, Inc., on Proposed Changes to Emergency Plans to Revise Emergency Action Levels for Arkansas; Grand Gulf; River Bend; and Waterford (EPID-L-2017-LRM-0060) ML16109A3642016-04-18018 April 2016 Summary of Meeting to Discuss Supplemental Inspection Results and Annual Assessment Meeting with Entergy Operations Inc. Regarding 2015 Performance of Arkansas Nuclear One ML15348A1882016-01-0606 January 2016 Summary of October 28, 2015, Closed Meeting Between Representatives of the U.S. Army Corps of Engineers, U.S. Nuclear Regulatory Commission and Entergy Nuclear Operations, Inc. to Discuss Flood Analysis Associated with Arkansas Nuclear One, ML15267A4182015-09-24024 September 2015 Summary of Meeting to Discuss Arkansas Nuclear One Performance Improvement ML15225A2542015-08-14014 August 2015 Summary of 4/20-23/2015 Audit in Support of Request to Adopt National Fire Protection Association NFPA 805, Performance-Based Standard for Fire Protection for LWR Generating Plants (2001 Edition) ML15132A1752015-05-21021 May 2015 Summary of Annual Assessment Meeting with Entergy Operations Inc., Regarding ANO 2014 Performance ML15089A1642015-04-27027 April 2015 Summary of February 25, 2015, Partially Closed Meeting with Industry Stakeholders Regarding the Babcock and Wilcox Loss of Coolant Accident Evaluation Model Analysis ML15007A4782015-01-15015 January 2015 Summary of July 15-18, 2013, Arkansas Nuclear One, Unit 2, Audit Associated with License Amendment Request to Transition to National Fire Protection Association Standard 805 ML14356A1722014-12-22022 December 2014 Summary of Site Audit to Support the Review of a License Amendment Request for Arkansas Nuclear One, Unit 2 to Transition to the National Fire Protection Association (NFPA) Standard 805 Fire Protection Licensing Basis ML14197A5832014-09-18018 September 2014 Summary of the June 19, 2014, Category 1 Public Meeting with Entergy to Discuss Seismic Hazard Reevaluations Associated with Implementation of Japan Lessons-Learned Near-Tear Task Force Recommendation 2.1 ML14259A5972014-09-16016 September 2014 Summary of Annual Performance Assessment Meeting for Arkansas Nuclear One Performance ML14213A4272014-09-12012 September 2014 Summary of July 16, 2014, Closed Meeting Between Representatives of the U.S. Army Corps of Engineers Nuclear Regulatory Commission, and Entergy Operations Inc. to Discuss Flooding Analysis Associated with Arkansas Nuclear One, Units 1 and 2 ML14162A3712014-06-26026 June 2014 5/22/2014 Summary of Meeting with Entergy Operations, Inc. to Discuss Flooding Hazard Reevaluation Extension Request for Arkansas Nuclear One, Units 1 and 2; Near-Term Task Force Recommendation 2.1 ML14170A0602014-06-23023 June 2014 Summary of 5/27/2014 Conference Call Regarding Refueling Outage Steam Generator Inspection ML14163A0502014-06-13013 June 2014 Summary of Conference Call with Arkansas Nuclear One, Unit 2, Regarding the Spring Steam Generator Inspections ML14128A5122014-05-0909 May 2014 Summary of Regulatory Conference to Discuss Safety Significance of Arkansas Nuclear One Unit 1 Dropped Stator ML13172A0292013-07-0909 July 2013 Summary of 5/10/2013 Conference Call with Entergy Operations, Inc., 2013 Steam Generator Tube Inspections at Arkansas Nuclear One, Unit 1 ML13142A2272013-05-22022 May 2013 Summary of Public Meeting to Discuss Results of Augmented Inspection at Arkansas Nuclear One ML13043A6112013-02-26026 February 2013 Summary of 1/25/2013 Conference Call Regarding the Upcoming 2013 Steam Generator Tube Inspections ML12276A3012012-10-12012 October 2012 Summary of October 25, November 8, and November 10, 2011, Conference Calls Related to Fall 2011 Refueling Outage Steam Generator Tube Inspections ML12275A5492012-10-0101 October 2012 Summary of Meeting with Entergy Operations, Inc., to Discuss the Performance of the Subject Facilities, Recent Organizational Changes, and Current Regulatory Issues ML12240A4162012-08-27027 August 2012 Public Meeting with Entergy Operations, Inc to Discuss the Performance of the Subject Facilities and Current Regulatory Issues ML12222A0312012-08-0808 August 2012 Arkansas Monitoring Call Summary ML12171A3662012-07-16016 July 2012 6/12-13/2012 Summary of Meeting at the Plant Site in Russellville, AR, to Discuss Entergy Operations, Inc.'S License Amendment Request to Adopt National Fire Protection Association (NFPA) Standard 805 at Arkansas Nuclear One, Unit 2 ML1202704162012-02-13013 February 2012 1/26/2012 - Summary of Meeting with Entergy and Exelon to Discuss Recent Once-Through Steam Generator Inservice Inspection Results 2024-04-18
[Table view] Category:Memoranda
MONTHYEARML24128A2402024-05-0808 May 2024 Entergy Operations, Inc. - Entergy Fleet Project Manager Assignment ML23047A3822023-03-21021 March 2023 Summary of December 15, 2022 Periodic Advanced Reactor Stakeholder Public Meeting ML22349A5052023-02-0808 February 2023 Results of a Reactor Oversight Process Self Assessment Effectiveness Review of the Recommendations from IP 95003 at Arkansas Nuclear One ML22147A0932022-06-0606 June 2022 2021 Annual Assessment Public Meeting Summary ML22034A3932022-02-16016 February 2022 Calendar Year 2021 Security Baseline Completion Memo ML21295A0882021-10-21021 October 2021 Fiscal Year 2021 Research and Test Reactors Inspection Program Completion Status ML21288A0392021-10-18018 October 2021 September 14, 2021, Summary of Public Workshop on Scale/Melcor Source Term Demonstration Project - Pebble-Bed Molten-Salt-Cooled Reactor ML21273A1772021-10-0101 October 2021 Fiscal Year 2021 Research and Test Reactors Inspection Program Completion Status ML21181A3352021-07-0101 July 2021 June 23, 2021, Summary of Public Meeting to Discuss Technology Inclusive Content of Application Project ML21158A2232021-06-0808 June 2021 Meeting Summary for Ticap Workshop 3 ML21140A3892021-05-24024 May 2021 Riv Column 1 EOC 2020 Public Meeting Summary ML21132A2952021-05-14014 May 2021 Summary of Public Meeting to Discuss Technology Inclusive Content of Application Project ML20337A1572020-12-0808 December 2020 Summary of Teleconference Meeting with Entergy Operations, Inc. to Discuss the Forthcoming Supplemental Response Concerning Generic Letter 2004-02 for Arkansas Nuclear One, Units 1 and 2 ML20149K5412020-11-23023 November 2020 Memo to File: Environmental Assessment and Finding of No Significant Impact and NRC Financial Analysis for Entergy Operations, Inc. Decommissioning Funding Plan Submitted in Accordance with 10 CFR 72.30(b) and (C) for Arkansas Nuclear One I ML20150A4212020-11-23023 November 2020 Memo to File: Environmental Assessment and Finding of No Significant Impact and NRC Financial Analysis for Entergy Nuclear Company, LLC Decommissioning Funding Plan Submitted in Accordance with 10 CFR 72.30(b) and (C) for Grand Gulf ISFSI ML19204A2972019-07-31031 July 2019 Memo to Management Review Board Arkansas Follow-up FY2019 Proposed Final Report ML18173A0082018-06-20020 June 2018 Cancelling Numerous Inspection Report Numbers ML17153A0012017-06-0606 June 2017 Staff Observations of Testing for Generic Safety Issue 191 During a May 10 to May 11, 2017, Trip to the Alden Test Facility for Control Components Inc. Strainer Tests ML16145A3392016-05-24024 May 2016 NRC Supplemental Inspection Procedure 95003 (Report - 05000313/2016007, and 05000368/2016007) List of Documents Reviewed ML16088A2042016-03-28028 March 2016 Memo T Bowers from s Ruffin, Technical Assistance Requests - Review 2015 Tri-Annual Decommissioning Funding Plans for Multiple Independent Spent Fuel Storage Installations W/ Encl 2 (Template) ML16088A2052016-03-28028 March 2016 Enclosure 1 - (72.30 DFP Reviews to Be Completed 2015) - Memo T Bowers from s Ruffin, Technial Assistance Requests - Review 2015 Tri-Annual Decommissioning Funding Plans for Multiple Independent Spent Fuel Storage Installations ML16076A2212016-03-16016 March 2016 NRC Supplemental Inspection Procedure 95003 (Report 05000313/2016007, 05000368/2016007) Request for Information ML16061A3622016-03-0101 March 2016 OEDO-15-00641 DPO-2015-001 on the Significance Determination Process Evaluation for a Finding at Arkansas Nuclear One Involving the March 2013, Unit 1 Stator Drop Event, Redacted-Public ML15292A2412015-10-21021 October 2015 October 28, 2015, Notice of Forthcoming Closed Meeting to Discuss Dam Failure Analysis for Arkansas Nuclear One, Units 1 and 2 ML15218A6042015-08-0606 August 2015 Inspection Procedure 95003 Communication Team Charter ML15089A1642015-04-27027 April 2015 Summary of February 25, 2015, Partially Closed Meeting with Industry Stakeholders Regarding the Babcock and Wilcox Loss of Coolant Accident Evaluation Model Analysis ML14356A1722014-12-22022 December 2014 Summary of Site Audit to Support the Review of a License Amendment Request for Arkansas Nuclear One, Unit 2 to Transition to the National Fire Protection Association (NFPA) Standard 805 Fire Protection Licensing Basis ML14351A2602014-12-19019 December 2014 Memo C K Bladey Re Notice of Issuance of Exemption from Holtec Intl CoC No. 1014 Fuel Specification and Loading Conditions at Arkansas Nuclear One ISFSI ML14356A5612014-12-17017 December 2014 Third-Party Assessment of Safety Culture ML14345B0652014-12-11011 December 2014 Memo C Bladey Re Federal Register Notice of Issuance of Environmental Assessment and Finding of No Significant Impact ANO Units 1 & 2 ISFSI 72-12 and 72-1014 ML14213A4272014-09-12012 September 2014 Summary of July 16, 2014, Closed Meeting Between Representatives of the U.S. Army Corps of Engineers Nuclear Regulatory Commission, and Entergy Operations Inc. to Discuss Flooding Analysis Associated with Arkansas Nuclear One, Units 1 and 2 ML14184B2432014-07-10010 July 2014 Notice of Forthcoming Closed Meeting to Discuss Dam Failure Analysis for Arkansas Nuclear One, Units 1 and 2 ML14163A0502014-06-13013 June 2014 Summary of Conference Call with Arkansas Nuclear One, Unit 2, Regarding the Spring Steam Generator Inspections ML13269A2082013-12-12012 December 2013 Cover Memo from B. Caldwell to M. Markley RAI for Arkansas Nuclear One (ANO) Revision 15 Security Plan Review ML13255A4872013-09-10010 September 2013 Request for Additional Information to Entergy Operations, Arkansas Nuclear One-Units 1 and 2, Regarding NTTF Recommendation 9.3 Phase 1 Staffing Assessment Submittal ML12324A4222012-11-14014 November 2012 Meeting Notice with Entergy Operations, Inc. to Discuss the Status of the Revised Application for Arkansas Nuclear One, Unit 2 to Transition to National Fire Protection Association (NFPA) Standard 805 ML12319A1222012-11-14014 November 2012 Notice of Forthcoming Meeting with Entergy Operations, Inc. to Discuss Resubmittal of License Amendment Request to Adopt National Fire Protection Association (NFPA) Standard 805 at Arkansas Nuclear One, Unit 2 ML12271A2482012-09-27027 September 2012 10/9/2012 Notice of Forthcoming Meeting with Entergy Operations, Inc. to Discuss Resubmittal of License Amendment Request to Adopt National Fire Protection Association (NFPA) Standard 805 at Arkansas Nuclear One, Unit 2 ML12166A1002012-06-18018 June 2012 Forthcoming Meeting on 6/29/12 with Entergy Operations, Inc. to Discuss License Amendment Request to Adopt National Fire Protection Association (NFPA) Standard 805 at Arkansas Nuclear One, Unit 2 ML1214600172012-05-30030 May 2012 June 12-13, 2012, Notice of Meeting at the Plant Site in Russellville, AR to Discuss Entergy Operations, Inc.'S License Amendment Request to Adopt National Fire Protection Association (NFPA) Standard 805 at Arkansas Nuclear One, Unit 2 ML1134801002011-12-19019 December 2011 Notice of Forthcoming Meeting with Exelon Generation Company, LLC, and Entergy Operations, Inc., to Discuss Steam Generator Inspection Results at Three Mile Island, Unit 1, and Arkansas Nuclear One, Unit 1 ML1116101632011-09-0707 September 2011 Review of Amendment 22 of Safety Analysis Report - Period from 10/6/2008 Through 3/18/2010 ML1123506752011-08-31031 August 2011 Notice of Meeting with Entergy Operations, Inc. to Discuss a Proposed License Amendment Request for Arkansas Nuclear One, Unit 2, for Its Revised Fuel Handling Accident (Fha) Analysis and Several Technical Specification Task Force Travel ML1115704052011-06-0606 June 2011 Notice of Meeting with Entergy Operations, Inc., to Discuss Implementation of Quality Oversight and Verification Programs at Entergy Sites Including Actions Being Taken to Enhance Effectiveness ML11116A0332011-04-29029 April 2011 Monthly Operating Reports for the 1st Quarter of 2011 ML1111009242011-04-29029 April 2011 Summary of 3/15/11 (P.M. Session) Meeting with Entergy Operations, Inc. to Discuss Arkansas Nuclear One, Unit 1 Planned License Amendment Request for Technical Specification Change Service Water System Related Support Features ML1109506462011-04-11011 April 2011 Verbal Authorization of Request for Alternative ANO1-R&R-015, Request for Use of Non-ASME Code Repair to Service Water Piping in Accordance with Generic Letter 90-05, Fourth 10-Year Interval ML1108804522011-03-30030 March 2011 Notice of Forthcoming Meeting with Entergy Operations, Inc., to Discuss Proposed License Amendment Request to Adopt NFPA 805 for Arkansas Nuclear One, Units 1 and 2 ML1107504052011-03-21021 March 2011 Notice of Meeting with Entergy Operations, Inc., to Discuss Fleetwide Submittal for Proposed Technical Specification and Quality Assurance Program Manual Changes Related to Unit Staff Qualification Requirements ML1106200032011-03-0303 March 2011 3/15/11 Notice of Forthcoming Meeting with Entergy Operations, Inc. to Discuss Arkansas Nuclear One, Unit 1 Planned License Amendment Request for Technical Specification Change Service Water System Related Support Features 2024-05-08
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June 13, 2014 MEMORANDUM TO: Michael T. Markley, Chief Plant Licensing Branch IV-1 Division of Operating Reactor Licensing Office of Nuclear Reactor Regulation FROM: Gloria J. Kulesa, Chief /RA/
Steam Generator Tube Integrity and Chemical Engineering Branch Division of Engineering Office of Nuclear Reactor Regulation
SUBJECT:
SUMMARY
OF CONFERENCE CALL WITH ARKANSAS NUCLEAR ONE, UNIT 2, REGARDING THE SPRING 2014 STEAM GENERATOR INSPECTIONS (TAC NO. MF3897)
On May 27, 2014, the staff of the Steam Generator Tube Integrity and Chemical Engineering Branch (ESGB) of the Division of Engineering participated in a conference call with representatives of Entergy Nuclear Operations, Inc. (the licensee) regarding the ongoing steam generator (SG) inspection activities at Arkansas Nuclear One, Unit 2. In support of the conference call, the licensee provided the document attached to the enclosed conference call summary. Please include Kenneth J. Karwoski, Andrew B. Johnson, and me on distribution of the final document. Please include me on concurrence only if you have made significant changes to the enclosed summary. Please close this TAC upon issuance of the enclosed summary.
ESGB formally reviews all SG inspection summary report(s) submitted by licensees in accordance with the plants technical specification (TS) requirements. The licensees submit the summary report(s) following the completion of the SG tube inspections at a frequency defined by their TSs. Therefore, please provide the report(s) and a work request to me when submitted.
The process for handling our review of SG inspection summary reports, as well as the SG conference calls, is outlined in a March 12, 2009, memo from Michele G. Evans to Joseph G. Giitter (Agencywide Documents Access and Management System Accession Number ML090710575). We appreciate your support in this matter.
Docket No. 50-368
Enclosure:
As stated CONTACT: Marioly Diaz Colon, NRR/DE 301-415-2849
June 13, 2014 MEMORANDUM TO: Michael T. Markley, Chief Plant Licensing Branch IV-1 Division of Operating Reactor Licensing Office of Nuclear Reactor Regulation FROM: Gloria J. Kulesa, Chief /RA/
Steam Generator Tube Integrity and Chemical Engineering Branch Division of Engineering Office of Nuclear Reactor Regulation
SUBJECT:
SUMMARY
OF CONFERENCE CALL WITH ARKANSAS NUCLEAR ONE, UNIT 2, REGARDING THE SPRING 2014 STEAM GENERATOR INSPECTIONS (TAC NO. MF3897)
On May 27, 2014, the staff of the Steam Generator Tube Integrity and Chemical Engineering Branch (ESGB) of the Division of Engineering participated in a conference call with representatives of Entergy Nuclear Operations, Inc. (the licensee) regarding the ongoing steam generator (SG) inspection activities at Arkansas Nuclear One, Unit 2. In support of the conference call, the licensee provided the document attached to the enclosed conference call summary. Please include Kenneth J. Karwoski, Andrew B. Johnson, and me on distribution of the final document. Please include me on concurrence only if you have made significant changes to the enclosed summary. Please close this TAC upon issuance of the enclosed summary.
ESGB formally reviews all SG inspection summary report(s) submitted by licensees in accordance with the plants technical specification (TS) requirements. The licensees submit the summary report(s) following the completion of the SG tube inspections at a frequency defined by their TSs. Therefore, please provide the report(s) and a work request to me when submitted.
The process for handling our review of SG inspection summary reports, as well as the SG conference calls, is outlined in a March 12, 2009, memo from Michele G. Evans to Joseph G. Giitter (Agencywide Documents Access and Management System Accession Number ML090710575). We appreciate your support in this matter.
Docket No. 50-368
Enclosure:
As stated CONTACT: Marioly Diaz Colon, NRR/DE 301-415-2849 DISTRIBUTION:
DE R/F EMurphy AObodoako RidsNrrPMArkansas JDrake ADAMS Accession Number: ML14163A050 OFFICE NRR/DE/ESGB NRR/DE/ESGB NRR/DE NRR/DE/ESGB NAME MDiaz-Colon AJohnson KKarwoski GKulesa DATE 06/ 12 /2014 06/ 12 /2014 06/ 12 /2014 06/ 13 /2014 OFFICIAL RECORD COPY
CONFERENCE CALL
SUMMARY
ARKANSAS NUCLEAR ONE, UNIT 2, REGARDING SPRING 2014 STEAM GENERATOR INSPECTIONS DOCKET NO. 50-368 TAC NO. MF3897 On May 27, 2014, the staff of the Steam Generator Tube Integrity and Chemical Engineering Branch (ESGB) of the Division of Engineering participated in a conference call with representatives of Entergy Nuclear Operations, Inc. (the licensee) regarding the ongoing steam generator (SG) inspection activities at Arkansas Nuclear One, Unit 2 (ANO-2). In support of the conference call, the licensee provided the document attached to this conference call summary.
Additional clarifying information not included in the document provided by the licensee is summarized below.
- ANO-2 replaced the original SGs with Westinghouse Model Delta 109 SGs. The replacement SGs have been in service for 14 calendar years. The fourth SG inservice inspections are being performed in the current refueling outage (refueling outage 23). The SGs are at the end of their first inspection interval defined by the technical specifications. ANO-2 has been inspecting the SGs every third refueling outage.
- In the ANO2 SG Primary to Secondary Leakrate (H-3) Gallons per Day (GPD) graph on page 7 of the attachment, the y-axis units are GPD.
- Verification of anti-vibration bar (AVB) positions will be performed with eddy current auto analysis after the SG tube inspections are complete. The estimated time to complete the verification is two weeks.
- The licensee confirmed that the reference Westinghouse letter to Entergy, MPENT-12-001 on page 2 of the attachment was referring to the Nuclear Safety Advisory Letter 12-01.
- The wear growth rate of the preliminary operational assessment for the current outage (at 95/50 probability/confidence interval values) is 4.5 percent.
- Plugging AVB indications greater than or equal to 30 percent through wall allows the licensee to operate on a three-cycle inspection schedule.
- No tube-to-tube wear was identified in the current outage.
- There were a total of 80 AVB indications in both SGs in the previous inspection.
- The inspections identified no wear associated with loose parts.
Enclosure
- The secondary side inspections performed in both SGs did not identify any erosion or cracks in the feed ring, primary or secondary steam separators, or the outlet venturi.
- The licensee clarified that the three machine remnants referenced on page 5 refer to very small machine turnings (i.e., lathe turning).
- An evaluation of blockage of the top support plate will be done as part of the eddy current auto-analysis that is verifying the position of the AVBs.
- At the time of the call, the licensee stated that approximately 100 percent of the eddy current analysis was complete and the AVB location analysis still had two weeks until completion.
- The licensee confirmed that the replacement SGs did not have a stay cylinder, that the center region formerly occupied by the stay cylinder had been filled in with tubes, and that there was a six-inch wide open lane in the middle of the replacement SGs.
The following abbreviations are used in the document provided by the licensee:
2R22 = Unit 2 Refueling Outage 22 ANO2 = Arkansas Nuclear One, Unit 2 CMOA = Conditional Monitoring Operational assessment CR-ANO-2-2014-01539 = Condition Report EPRI = Electric Power Research Institute ETSS = examination technique specification sheet NEI 97-06 = Nuclear Energy Institute Steam Generator Program Guidelines N/A = not applicable NDE = nondestructive evaluation PWR = pressurized water reactor REV = Revision TTS = Top of tubesheet The staff did not identify any issues that required follow-up action at this time; however, the staff asked to be notified in the event that any unusual conditions were detected during the remainder of the outage.