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{{#Wiki_filter:ACCELERATED DISIKBUTION DEMONSTRA.TION SYSTEM REGULAT INFORMATION DISTRIBUTION+STEM (RIDE)ACCESSION NBR:8903220424 DOC.DATE: 89/03/14 NOTARIZED:
{{#Wiki_filter:ACCELERATED             DISIKBUTION             DEMONSTRA.TION             SYSTEM REGULAT     INFORMATION DISTRIBUTION+STEM (RIDE)
NO DOCKET FACIL:50-4lg Beaver Valley Power Station, Unit 2, Duquesne Light C 05000412 AUTH.NAME AUTHOR AFFILIATION NOONANFT.P.
ACCESSION NBR:8903220424           DOC.DATE: 89/03/14       NOTARIZED: NO             DOCKET FACIL:50-4lg Beaver Valley Power Station, Unit 2, Duquesne Light                   C 05000412 AUTH. NAME           AUTHOR   AFFILIATION NOONANFT.P.           Duquesne Light Co.
Duquesne Light Co.RECIP.NAME RECIPIENT AFFILIATION
RECIP.NAME           RECIPIENT AFFILIATION


==SUBJECT:==
==SUBJECT:==
LER 89-003-00:on 890212,reactor tripped due to main feedwater regulating valve failure.W/890314 ltr.W/8 DISTRIBUTION CODE: IE22D COPIES RECEIVED:LTR t ENCL I SIZE: TITLE: 50.73 Licensee Event Report (LER), Incident Rpt, etc.NOTES:LPDR 2cys Transcripts.
LER   89-003-00:on 890212,reactor tripped due to main feedwater regulating valve failure.W/890314 ltr.
LPDR 2cys PDR Documents.
W/8 DISTRIBUTION CODE: IE22D COPIES RECEIVED:LTR t ENCL I SIZE:
Application for permit renewal filed.05000412 RECIPIENT ID CODE/NAME PDl-4 LA TAMFP INTERNAL: ACRS MICHELSON ACRS WYLIE AEOD/DSP/TPAB ARM/DCTS/DAB NRR/DEST/ADE 8H NRR/DEST/CEB 8H NRR/DEST/ICSB 7 NRR/DEST/MTB 9H.NRR/DEST/RSB 8E NRR/DLPQ/HFB 10 NRR/DOEA/EAB 11 NRR/DREP/RPB 10 NUDOCS-ABSTRACT RES/DSIR/EIB RGN1 FILE 01 EXTERNAL: EGSG WILLIAMSFS H ST LOBBY WARD NRC PDR NSIC MURPHYFG.A NOTES: COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 2 2 1 1 1 1 1 1 4 4 1 1 1'1 1 2 2 RECIPIENT ID CODE/NAME PD1-4 PD ACRS MOELLER AEOD/DOA AEOD/ROAB/DSP DEDRO NRR/DEST/ADS 7E NRR/DEST/ESB 8D NRR/DEST/MEB 9H NRR/DEST/PSB 8D NRR/DEST/SGB 8D NRR/DLPQ/QAB 10 NRR/DREP/RAB 10 NRRJ3/SIB 9A REG Fjj 02 RES/DSR/FRAB FORD BLDG HOYFA LPDR NSIC MAYSFG COPIES LTTR ENCL 1 1 2 2 1 1 2 2 1 1 1 0 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 NOZE'IO ALL'RIDS" RICIPZEPIS:
TITLE: 50.73 Licensee Event Report (LER), Incident Rpt, etc.
PIZASE HELP US IO IlEDUCE%ASTl CGKPACT IHE DCjCUNE&#xc3;Z CG&#xc3;IK)L DESKF ROC'l-37 (EXT.20079)%0 EIZKBRXS YOUR MHB HKH DISTBZBUTICN LIBTS FOR DOC(IMENIS YOU DQHFT NEED<TOTAL NUMBER OF COPIES REQUIRED: LTTR 47 ENCL 46  
NOTES:LPDR 2cys     Transcripts. LPDR 2cys PDR Documents.                             05000412 Application for permit renewal filed.
RECIPIENT          COPIES              RECIPIENT           COPIES ID CODE/NAME         LTTR ENCL          ID CODE/NAME        LTTR ENCL PDl-4 LA                 1      1      PD1-4 PD                1    1 TAMFP                     1      1 INTERNAL: ACRS MICHELSON             1      1      ACRS MOELLER            2    2 ACRS WYLIE               1      1      AEOD/DOA                1    1 AEOD/DSP/TPAB             1      1      AEOD/ROAB/DSP            2    2 ARM/DCTS/DAB             1      1      DEDRO                    1    1 NRR/DEST/ADE 8H           1      1      NRR/DEST/ADS    7E      1    0 NRR/DEST/CEB 8H          1      1      NRR/DEST/ESB    8D      1    1 NRR/DEST/ICSB 7          1      1      NRR/DEST/MEB    9H      1    1 NRR/DEST/MTB 9H          1      1      NRR/DEST/PSB    8D      1   1
          .
NRR/DEST/RSB 8E          1      1      NRR/DEST/SGB    8D       1    1 NRR/DLPQ/HFB 10          1      1      NRR/DLPQ/QAB    10      1    1 NRR/DOEA/EAB 11          1      1      NRR/DREP/RAB    10       1    1 NRR/DREP/RPB 10           2      2      NRRJ3     /SIB 9A       1    1 NUDOCS-ABSTRACT          1      1      REG Fjj       02       1    1 RES/DSIR/EIB              1      1      RES/DSR/FRAB             1   1 RGN1      FILE 01        1       1 EXTERNAL: EGSG WILLIAMSFS            4      4      FORD BLDG HOYFA          1     1 H ST LOBBY WARD          1       1     LPDR                    1     1 NRC PDR                  1   '        NSIC MAYSFG              1     1 NSIC MURPHYFG.A          1       1 NOTES:                                2      2 NOZE 'IO ALL 'RIDS" RICIPZEPIS:
PIZASE HELP US IO IlEDUCE %ASTl   CGKPACT IHE DCjCUNE&#xc3;Z CG&#xc3;IK)L DESKF ROC'l-37   (EXT. 20079) %0 EIZKBRXS YOUR MHB HKH DISTBZBUTICN LIBTS FOR DOC(IMENIS   YOU DQHFT NEED<
TOTAL NUMBER OF COPIES REQUIRED: LTTR               47   ENCL     46


NRC Form 388 (9.83)I(LICENSEE EVENT REPORT ILER)U.S.NUCLEAR REGULATORY COMMISSION APPROVEO OMB NO.31504104 EXPIRES: 8/31/88 F AC I LIT Y N A ME I I I TITLE (4)Reactor Trip Due to Main Feedwater Regulating Valve Failure DOCKET NUMBER (2)0 5 0 0 0 PAGE 3/1 OF 0 FVENT DATE (5)LER NUMBER (5)REPORT DATE I7)OTHER FACILI'TIFS INVOLVED (8)MONTH OAY YEAR YEAR SEGVENTIAL NVMSEA yh'.REVISION'Ai NUMBER MONTH OAY YEAR FACILITY NAMES DOCKET NUMBER(s)0 5 0 0 0 212 89 89 003 0 0 03 4 89 N/A 0 5 0 0 0 OPERATING MODE (SI POWE R LEYEL P 5 5 (10)5?'PNryr'Q?y r'rc'yvynHX rg?e"@.gp.'0.402(bl 20.405(el(I i(i)20.405(e l(1)(ii)20.405(e I)I I (ii))20.405(~l(l)I Iv)20.405(~l(1)(vl 20A05(cl 50.35(cl(II 50.35 Ic I (2)50 73(el(2)li)d0.73(~l(2)(i/I 50.73(e)(2 I (iii)LICENSEE CONTACT FOR THIS LER (12)50.73(e)(2)(iv)50.73(~)(2)(v)50,73(~)(21(viil 50.73(~)(2)(wii)IAI 50.73(~)12)(wii)IBI 50.73(~)(2)(rrl 0 THE REOUIREMENTS OF 10 CFR (I:/Check one or morc OI tnc IoliowrnP/
NRC Form 388                                                                                                                                     U.S. NUCLEAR REGULATORY COMMISSION (9.83)
(11)THIS REPORT IS SUBMITTED PURSUANT T 73.71(b)73.71Icl OTHER/Spetiry In AprrreCt oe/ow enriin Tert, NIIC Form 366AI NAME Mr.Thomas P.Noonan, Plant Manager TELEPHONE NUMBER AREA CODE 41 264 3-1 25 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE OESCRIBEO IN THIS REPORT (13)CAUSE SYSTEM COMPONENT MANUFAC.TURER REPORTABLE p CAUSE SYSTEM COMPONENT MANVFAC.TVRER X JB FCV C63 5 Y$P:,"'''.'SVPPLEMEN1'AL REPORT EXPECTFD (14)YES//I ycr, comp/etc EXPECTED SU84IISSIOIY DATE/ABSTRACT ILimrt to/400 rpeccr./c,, epprovimeteiy
I(                                                                                                                                                               APPROVEO OMB NO. 31504104 LICENSEE EVENT REPORT ILER)                                                         EXPIRES: 8/31/88 F AC I LITY N A   ME III                                                                                                                DOCKET NUMBER (2)                            PAGE 3/
/i/teen r/nple torte tyPcwrinen
0  5    0      0      0                1    OF  0 TITLE (4)
/inn/l(d)EXPECTED SU 8 M I SS I 0 N DATE (15I MONTH OAY YEAR NRC Form 358 (9 83)On 2/12/89, with the Unit in Power Operation, a power reduction from 904 reactor power to 50%reactor power was in progress as part of End of Core Life programs.At 0048 hours, operators noticed erratic operation of the"C" Main Feedwater Regulating Valve (MFRV).The operators placed the"C" MFRV in manual to control steam generator level.At 0108 hours at approximately 55~reactor power, the"A" Main Feedwater Pump was shutdown to reduce the pressure differential across the valve allowing easier valve movement and control.At 0120 hours, a turbine trip/reactor trip occurred due to a high water level in the"C" steam generator.
Reactor Trip                   Due     to Main Feedwater Regulating Valve Failure FVENT DATE (5)                         LER NUMBER (5)                       REPORT DATE I7)                         OTHER FACILI'TIFS INVOLVED (8)
The operators stabilized the plant in Hot Shutdown utilizing the Emergency Operating Procedures.
SEGVENTIAL yh'. REVISION MONTH                                   FACILITYNAMES                            DOCKET NUMBER(s)
The HC" MFRV was found to have sheared anti-rotation pins and the stem detached from the valve plug.The cause for the valve failure was attributed to hydraulic forces and vibration acting over time.The MFRVs were all disassembled, inspected and repaired as necessary.
MONTH        OAY        YEAR      YEAR              NVMSEA    'Ai NUMBER                    OAY  YEAR 0   5   0     0   0 212 89 89                                   003             0   0   03                   4 89               N/A                                   0   5   0   0     0 THIS REPORT IS SUBMITTED PURSUANT T0 THE REOUIREMENTS OF 10 CFR (I: /Check one or morc OI tnc IoliowrnP/ (11)
This event was reported to the Nuclear Regulatory Commission at 0300 hours, in accordance with 10CFR50.72.b.2.ii.
OPERATING POWE R
There were no safety implications to the public as a result of this event.This type of event has previously been analyzed as stated in the Updated Final Safety Analysis Report, Section 15.1.2,"Feedwater System Malfunctions Causing an Increase In Feedwater Flow".8903220424 8903i4$)PDR ADOCK 05000412 S PNU  
                  '0.402(bl MODE (SI 20.405(el(I i(i) 20A05(cl 50.35(cl(II 50.73(e) (2)(iv) 50.73( ~ )(2)(v) 73.71(b) 73.71Icl LEYEL (10)         P 5 5              20.405(e l(1) (ii)                      50.35 Ic I (2)                     50,73( ~ ) (21(viil                            OTHER /Spetiry In AprrreCt
                    'rc 'yvynHX rg?e                                                                                                                                  oe/ow enriin Tert, NIIC Form 5?'PNryr'Q?y r                          20.405(e I) I I (ii))                   50 73(el(2) li)                     50.73( ~ )(2)(wii)IAI                          366AI 20.405( ~ l(l) I Iv)                   d0.73( ~ l(2)(i/I                  50.73( ~ )12)(wii)IBI
          "@. gp.
20.405( ~ l(1) (vl                      50.73(e)  (2 I (iii)              50.73( ~ )(2)(rrl LICENSEE CONTACT FOR THIS LER (12)
NAME                                                                                                                                                         TELEPHONE NUMBER AREA CODE Mr. Thomas P. Noonan, Plant Manager                                                                                                       41 264                     3-1           25 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE OESCRIBEO IN THIS REPORT (13)
MANUFAC.          REPORTABLE                                                                MANVFAC.
CAUSE     SYSTEM       COMPONENT                                           p                       CAUSE SYSTEM COMPONENT TURER                                                                                      TVRER X       JB                   FCV C63                       5     Y
                                                                                                                                                                                  $ P:, "'''. '
SVPPLEMEN1'AL REPORT EXPECTFD (14)                                                                             MONTH      OAY    YEAR EXPECTED SU 8 M I SS I 0N DATE (15I YES //I ycr, comp/etc   EXPECTED SU84IISSIOIY DATE/
ABSTRACT ILimrt to /400 rpeccr. /c,, epprovimeteiy /i/teen r/nple torte tyPcwrinen     /inn/ l(d)
On         2/12/89,                     with the Unit in Power Operation, a power reduction from             904         reactor power to 50% reactor power was in progress as part of End of Core Life programs. At 0048 hours, operators noticed erratic operation of the "C" Main Feedwater Regulating Valve (MFRV). The operators placed the "C" MFRV in manual to control steam generator level. At 0108 hours at approximately 55~ reactor                               power, the "A" Main Feedwater Pump was shutdown to reduce the pressure differential across the valve allowing easier valve movement and control. At 0120 hours, a turbine trip/reactor trip occurred due to a high water level in the "C" steam generator.                                 The operators                           stabilized the plant in Hot Shutdown utilizing the Emergency Operating Procedures. The HC" MFRV was                       found to have sheared anti-rotation pins and the stem detached                   from the valve plug. The cause for the valve failure was attributed to hydraulic forces and vibration acting over time. The MFRVs were all disassembled, inspected and repaired as necessary.                       This event was reported to the Nuclear Regulatory Commission at 0300 hours, in accordance with 10CFR50.72.b.2.ii.
There were no safety implications to the public as a result of this event. This type of event has previously been analyzed as stated in the Updated Final Safety Analysis Report, Section 15.1.2, "Feedwater System Malfunctions Causing an Increase In Feedwater Flow".
8903220424 8903i4                                                                                                                               $)
NRC Form 358 PDR             ADOCK 05000412 (9 83)                                S                                   PNU


NRC Form 3SSA (943)LICENSEE E ENT REPORT ILER)TEXT CONTINUATION U.S.NUCLEAR RFOULATORY COMMISSION APPROVED OMB NO.3150-CI04 EXPIRES: 8/3)/88 FACILITY NAME<<I DOCKET NUMBER)2I LER NUMBER)8)i+: SEQUENTIAL SFI NUMS 8 rr RFVISION NUMBER PAGE)3)Beaver Valley Power Station, Unit 2 p p p p p 4 1 2 TEXT///rrroro H>>co/r roqo/rod.o>>odd/I/orM/HRC Form36548l
NRC Form 3SSA                                                                                                   U.S. NUCLEAR RFOULATORY COMMISSION (943)
<<7)8 9 0 0 3 00 02 QF 0 4 DESCRIPTION On 2/12/89, with the Unit in Power Operation (Operating Mode 1), Operations personnel were reducing reactor power from 90%to 50<as part of End of Core Life programs.Prior to the Operating crew assuming the shift at 2300 hours on 2/11/89, the<<B<<Main Feedwater Regulating Valve (MFRV)had previously exhibited erratic valve control for steam generator water level.The<<B<<MFRV was in the automatic mode, however, the valve was not controlling smoothly.At 0048 hours, operators noticed erratic operation of the<<C<<MFRV.At 0108 hours, at approximately 554 power, the<<A<<Main Feedwater Pump was shutdown.At 0120 hours, the water level in the<<C<<steam generator increased to the high-high level setpoint (75%)causing.a turbine trip and feedwater isolation signal.The turbine trip caused a reactor trip, since reactor power was above the trip permissive of 49'.The feedwater isolation signal caused the following actions to occur: 1)trip of the running main feedwater pump, 2)auto-start of the auxiliary feedwater pumps, and 3)closure of the main feedwater regulating valves and bypass valves.Following the reactor trip, the operators utilized the Emergency Operating Procedures (E-0"Reactor Trip or Safety Injection<<
LICENSEE       E   ENT REPORT ILER) TEXT CONTINUATION                       APPROVED OMB NO. 3150-CI04 EXPIRES: 8/3)/88 FACILITY NAME <<I                                                       DOCKET NUMBER )2I             LER NUMBER )8)                        PAGE )3) i+: SEQUENTIAL       RFVISION SFI   NUMS 8 rr       NUMBER Beaver           Valley Power Station, Unit                     2   p p   p p   p 4 1 2 8 9      0 0        3      00 02            QF  0    4 TEXT ///rrroro H>>co /r roqo/rod. o>> odd/I/orM/HRC Form36548l <<7)
and ES-0.1"Reactor Trip Response")to stabilize the plant in Hot Standby (Operating Mode 3).APPARENT CAUSE OF THE EVENT The cause for this event was attributed to the failure of the<<C<<Main.Feedwater Regulating Valve (2FHS*FCV498).
DESCRIPTION On         2/12/89, with the Unit in Power Operation (Operating Mode 1),
This valve is a Copes-Vulcan, Model No.D-100-160, Part No.16-FA37RG.
Operations personnel were reducing reactor power from 90% to 50<
The valve failure was attributed to the hydraulic forces and vibration, which over time, mechanically excite the valve, damaging the anti-rotation cage slots, plug guides, retaining pins and valve stem.The<<B<<Main Feedwater Regulating Valve was found to have damaged anti-rotation pins.Nr)C FORM 300A IS 83)'U.S~CPCI)988-33<')09 000)0  
as part of End of Core Life programs.                                         Prior to the Operating crew assuming the shift at 2300 hours on 2/11/89, the <<B<< Main Feedwater                     Regulating Valve (MFRV) had previously exhibited erratic valve control for steam generator water level. The <<B<<
MFRV was                     in the automatic mode, however, the valve was not controlling smoothly. At 0048 hours, operators noticed erratic operation of the <<C<< MFRV. At 0108 hours, at approximately 554 power, the <<A<< Main Feedwater Pump was shutdown. At 0120 hours, the water level in the <<C<< steam generator increased to the high-high level setpoint (75%) causing. a turbine trip and feedwater isolation signal.                                     The turbine trip caused a reactor trip, since reactor power was above the trip permissive of 49'.
The feedwater                           isolation signal caused the following actions to occur:                       1)     trip of the running main feedwater pump, 2) auto-start of the auxiliary feedwater pumps, and 3) closure of the             main           feedwater           regulating valves and bypass valves.
Following the reactor trip, the operators utilized the Emergency Operating Procedures (E-0 "Reactor Trip or Safety Injection<< and ES-0.1 "Reactor Trip Response" ) to stabilize the plant in Hot Standby (Operating Mode 3).
APPARENT CAUSE OF THE EVENT The           cause           for this event was attributed to the failure of the
                <<C<<           Main. Feedwater Regulating Valve (2FHS*FCV498). This valve is         a Copes-Vulcan, Model No. D-100-160, Part No. 16-FA37RG.                                                   The valve               failure was attributed to the hydraulic forces and vibration, which over time, mechanically excite the valve, damaging the anti-rotation cage slots, plug guides, retaining pins and valve stem.                                 The <<B<< Main Feedwater Regulating Valve was found to have damaged anti-rotation pins.
Nr)C FORM 300A                                                                                                             'U.S ~ CPCI )988-33<' )09 000)0 IS 83)


NRC Form 366A 194)3)LICENSEE ENT REPORT (LERI TEXT CONTINUA ON U.S.NUCLEAR REGULATORY COMMISSION APPROVED OMB NO.3160&)04 EXPIRES: 8/31/88 FACILITY NAME (1)DOCKET NUMBER (2)YEAR LER NUMBER (6)SEQUENTIAL
NRC Form 366A                                                                                                       U.S. NUCLEAR REGULATORY COMMISSION 194)3)
+"'2 REVISION NVM8ER):.1 NUMSSR PAGE (3)Beaver Valley Power Station, Unit 2 o s o o o 4 1 2 8 9 TEXT/lf moro spinto/4 rtr)o/rod, oto tddr)/ono/IVRC Form 3664'4/OS)0 0 3 0 0 03oF 0 4 CORRECTIVE ACTIONS The following corrective actions were taken as a result of this event: Immediate:
LICENSEE               ENT REPORT (LERI TEXT CONTINUA ON                       APPROVED OMB NO. 3160&)04 EXPIRES: 8/31/88 FACILITY NAME (1)                                                             DOCKET NUMBER (2)             LER NUMBER (6)                     PAGE (3)
1).Operations personnel utilized the Emergency Operating Procedures to stabilize the plant in Hot Standby.2).The main feedwater regulating valves were disassembled and inspected.
YEAR    SEQUENTIAL +"'2 REVISION NVM8ER ):. 1 NUMSSR spinto Beaver Valley Power                         Station, Unit         2   o   s   o o   o 4 1 2 8 9     0 0    3        0 0      03oF        0      4 TEXT /lfmoro        /4 rtr)o/rod, oto tddr)/ono/IVRC Form 3664'4/ OS)
The anti-rotation pins were replaced on all main feedwater regulating valves.Long-term:
CORRECTIVE ACTIONS The             following corrective actions were taken                                 as a   result of this event:
An Engineering Memorandum has been generated requesting Engineering to identify an actuator and valve design which will eliminate the main feedwater regulating valve problems due to the hydraulic forces and vibration which over time, progressively damage the valves.2).All three steam generators will be inspected during the First Refueling Outage for potent'ial loose objects.SAFETY IMPLICATIONS There were no safety implications to the public as a result of this event.This type of event has previously been analyzed as stated in the Updated Final Safety Analysis Report (UFSAR), Section 15.1.2,"Feedwater System Malfunctions Causing an Increase in Feedwater Flow".Additionally, all the required Engineered Safety Features (ESF)system components actuated as follows as a result of the steam generator high-high water level condition 1).Turbine trip, causing a reactor trip because reactor power was greater than the P-9 trip permissive, 2).Feedwater following:
Immediate:
Isolation (FWI)signal, causing the NRC FORM 34OA (94)3)A).Trip of the running main feedwater pump, B).Automatic start of the auxiliary feedwater pumps 2FWE*P22, 23A and 23B), C).Closure of the main feedwater regulating valves and bypass valves.~V.S.CPOI)988-920-889
1).           Operations personnel utilized the Emergency Operating Procedures to stabilize the plant in Hot Standby.
~OOOTO  
2).           The         main         feedwater regulating valves were disassembled and         inspected. The anti-rotation pins were replaced on all     main feedwater regulating valves.
Long-term:
An       Engineering Memorandum has been generated requesting Engineering to identify an actuator and valve design which will eliminate the main feedwater regulating valve problems                       due     to the hydraulic forces and vibration which over time, progressively damage the valves.
2).           All three steam generators will be inspected during the First Refueling Outage for potent'ial loose objects.
SAFETY IMPLICATIONS There               were no safety implications to the public as a result of this event. This type of event has previously been analyzed as stated in the Updated Final Safety Analysis Report (UFSAR),
Section                       15.1.2,               "Feedwater System Malfunctions Causing an Increase in Feedwater Flow".                                               Additionally, all the required Engineered Safety Features                                         (ESF) system components actuated as follows as a result of the steam generator high-high water level condition 1). Turbine                         trip,     causing a reactor trip because reactor power was               greater than the P-9 trip permissive, 2).           Feedwater                   Isolation (FWI) signal,                   causing                 the following:
A). Trip of the running main feedwater pump, B). Automatic start of the auxiliary feedwater pumps 2FWE*P22, 23A and 23B),
C). Closure of the main feedwater regulating valves and bypass valves.
NRC FORM 34OA                                                                                                                  ~ V.S. CPOI )988-920-889 ~ OOOTO (94)3)


NRC Form 388A (94)3)LICENSEE ENT REPORT ILER)TEXT CONTINUA ON V.S.NUCLEAR REGULATORY COMMISSION APPROVED OMB NO.3)50&)04 EXPIRES: 8/31/88 FACILITY NAME (I)DOCKET NUMBER (2)LER NUMBER (8)YEAR gg SEOUENTIAL PP?r NUMBER.Rrr.REvrsKIN NUMBER PAGE (3)8eaver gal le Power Station, Unit 2 o s o o o 4 1 2 TEXT III moro Z>>oo/4 re/rr/rod, Iroo EdcNane/HRC
NRC Form 388A                                                                                                       V.S. NUCLEAR REGULATORY COMMISSION (94)3)
%%dmr 3684 9/lll)8 9 003 0 0 0 4 OF 0 4 In addition, the Nuclear Steam System Supplier (NSSS)has evaluated the utility's engineering interpretation of the Steam Generator Parametric Loose Object Licensing Report (WCAP-12101), which addressed the safety significance of the potential loose part (anti-rotation pin from 2FWS*FCV498) which could be trapped in the"C" steam generator tubesheet annulus.It was concluded that the estimated time required for the loose object to wear into a tube to the minimum allowable wall thickness, is 2.4 years.The NSSS concurred with this safety evaluation justifying continued operation of the remaining operating cycle.REPORTABI LITY This event was reported to the Nuclear Regulatory Commission at 0300 hours in accordance with 10CFR50.72.b.2.ii.
LICENSEE               ENT REPORT ILER) TEXT CONTINUA ON                         APPROVED OMB NO. 3)50&)04 EXPIRES: 8/31/88 FACILITY NAME (I)                                                           DOCKET NUMBER (2)             LER NUMBER (8)                     PAGE (3)
This written report is being provided in accordance with 10CFR50.73.a.2.iv, as an event involving a reactor protection system (RPS)or engineered safety fea'tures (ESF)system actuation.
SEOUENTIAL PP?r REvrsKIN YEAR gg    NUMBER   .Rrr. NUMBER 8eaver gal le                 Power     Station, Unit           2   o   s   o o   o 4 1 2 8  9      003              0    0 0      4 OF 0      4 TEXT IIImoro Z>>oo /4 re/rr/rod, Iroo EdcNane/HRC %%dmr 3684 9/ lll)
PREVIOUS OCCURRENCES There have been no previous Licensee Event Reports issued on this type of event/equipment failure at Beaver Valley Power Station Unit 2.NRC FORM 388A l94)3)AU.S.GPOr IOSS SSB SSP I)0r)10  
In addition, the Nuclear Steam System Supplier (NSSS) has evaluated                     the utility's engineering interpretation of the Steam Generator                     Parametric Loose Object Licensing Report (WCAP-12101),
which addressed                                 the safety significance of the potential loose part (anti-rotation pin from 2FWS*FCV498) which could be trapped in the "C" steam generator tubesheet annulus. It was concluded that the estimated time required for the loose object to wear into a tube to the minimum allowable wall thickness, is 2.4 years.                           The             NSSS   concurred with this safety evaluation justifying continued operation of the remaining operating cycle.
REPORTABI LITY This               event         was       reported to the Nuclear Regulatory Commission at 0300               hours         in accordance with 10CFR50.72.b.2.ii. This written report is being provided in accordance with 10CFR50.73.a.2.iv, as an event involving a reactor protection system (RPS) or engineered safety fea'tures (ESF) system actuation.
PREVIOUS OCCURRENCES There                 have         been             no previous       Licensee Event Reports issued on this type of event/equipment                                         failure at         Beaver Valley Power Station Unit 2.
NRC FORM 388A                                                                                                                   AU.S. GPOr IOSS SSB SSP I)0r)10 l94)3)


gled~Duquesne lt Nuclear Group P,O, Box 4 Shippingporh PA 15077~TelephOne (412)393-6000 March 14, 1989 ND3SPM:0422 Beaver Valley Power Station, Unit No.2 Docket No.50-412, License No.NPF-73 LER 89-003-00 United States Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Gentlemen:
gled~
In accordance with Appendix A, Beaver Valley Technical Specifications, the following Licensee Event Report is submitted:
Duquesne Nuclear Group lt                                    TelephOne (412) 393-6000 P,O, Box 4 Shippingporh PA 15077~
LER 89-003-00, 10 CFR 50.73 a.2.iv,"Reactor Trip Due to Main Feedwater Regulating Valve Failure".Very truly yours, T.P.Noonan Plant Manager vhy Attachment  
March 14, 1989 ND3SPM:0422 Beaver Valley Power Station, Unit No. 2 Docket No. 50-412, License No. NPF-73 LER 89-003-00 United States Nuclear Regulatory Commission Document Control Desk Washington,         DC 20555 Gentlemen:
In accordance with Appendix A, Beaver Valley Technical Specifications,           the   following Licensee     Event       Report is submitted:
LER 89-003-00,         10 CFR 50.73 a.2.iv, "Reactor Trip     Due     to Main Feedwater Regulating Valve Failure".
Very truly yours, T. P. Noonan Plant Manager vhy Attachment
 
March 14, 1989 ND3SPM'0422 Page two CC:  Mr. William T. Russell Regional Administrator United States Nuclear Regulatory Commission Region  1 475  Allendale Rd.
King of Prussia, PA      19406 C. A. Roteck, Ohio Edison Mr. Peter Tam,    BVPS Licensing Project Manager United  States  Nuclear  Regulatory Commission Washington, DC 20555 J. Beall, Nuclear Regulatory Commission, BVPS Senior Resident Inspector Mr. Alex Timme,    CAPCO  Nuclear Projects Coordinator Toledo Edison INPO Records  Center Suite  1500 1100 Circle  75 Parkway Atlanta, GA    30339 G. E. Muckle, Factory Mutual Engineering, Pittsburgh Mr. J. N. Steinmetz, Operating Plant Projects Manager Mid Atlantic Area Westinghouse Electric Corporation Energy Systems Service Division Box 355 Pittsburgh,  PA  15230 American Nuclear Insurers c/o Dottie Sherman, ANI    Library The Exchange Suite 245 270 Farmington Avenue Farmington, CT 06032 Mr. Richard Janati Department of Environmental Resources P. O. Box 2063 16th Floor, Fulton Building
* Harrisburg, PA 17120 Director, Safety Evaluation    &  Control Virginia Electric    6 Power Co.
P.O. Box 26666 One James  River Plaza Richmond, VA 23261


March 14, 1989 ND3SPM'0422 Page two CC: Mr.William T.Russell Regional Administrator United States Nuclear Regulatory Commission Region 1 475 Allendale Rd.King of Prussia, PA 19406 C.A.Roteck, Ohio Edison Mr.Peter Tam, BVPS Licensing Project Manager United States Nuclear Regulatory Commission Washington, DC 20555 J.Beall, Nuclear Regulatory Commission, BVPS Senior Resident Inspector Mr.Alex Timme, CAPCO Nuclear Projects Coordinator Toledo Edison INPO Records Center Suite 1500 1100 Circle 75 Parkway Atlanta, GA 30339 G.E.Muckle, Factory Mutual Engineering, Pittsburgh Mr.J.N.Steinmetz, Operating Plant Projects Manager Mid Atlantic Area Westinghouse Electric Corporation Energy Systems Service Division Box 355 Pittsburgh, PA 15230 American Nuclear Insurers c/o Dottie Sherman, ANI Library The Exchange Suite 245 270 Farmington Avenue Farmington, CT 06032 Mr.Richard Janati Department of Environmental Resources P.O.Box 2063 16th Floor, Fulton Building*Harrisburg, PA 17120 Director, Safety Evaluation
&Control Virginia Electric 6 Power Co.P.O.Box 26666 One James River Plaza Richmond, VA 23261
,/}}
,/}}

Revision as of 22:37, 21 October 2019

LER 89-003-00:on 890212,noticed Erratic Operation of Main Feedwater Regulating Valve C & Turbine Trip/Reactor Trip Occurred Due to High Water Level in Steam Generator C.Caused by Valve Vibration & Hydraulic forces.W/890314 Ltr
ML18041A188
Person / Time
Site: Beaver Valley
Issue date: 03/14/1989
From: Noonan T
DUQUESNE LIGHT CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
LER-89-003, LER-89-3, ND3SPM:0422, ND3SPM:422, NUDOCS 8903220424
Download: ML18041A188 (14)


Text

ACCELERATED DISIKBUTION DEMONSTRA.TION SYSTEM REGULAT INFORMATION DISTRIBUTION+STEM (RIDE)

ACCESSION NBR:8903220424 DOC.DATE: 89/03/14 NOTARIZED: NO DOCKET FACIL:50-4lg Beaver Valley Power Station, Unit 2, Duquesne Light C 05000412 AUTH. NAME AUTHOR AFFILIATION NOONANFT.P. Duquesne Light Co.

RECIP.NAME RECIPIENT AFFILIATION

SUBJECT:

LER 89-003-00:on 890212,reactor tripped due to main feedwater regulating valve failure.W/890314 ltr.

W/8 DISTRIBUTION CODE: IE22D COPIES RECEIVED:LTR t ENCL I SIZE:

TITLE: 50.73 Licensee Event Report (LER), Incident Rpt, etc.

NOTES:LPDR 2cys Transcripts. LPDR 2cys PDR Documents. 05000412 Application for permit renewal filed.

RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PDl-4 LA 1 1 PD1-4 PD 1 1 TAMFP 1 1 INTERNAL: ACRS MICHELSON 1 1 ACRS MOELLER 2 2 ACRS WYLIE 1 1 AEOD/DOA 1 1 AEOD/DSP/TPAB 1 1 AEOD/ROAB/DSP 2 2 ARM/DCTS/DAB 1 1 DEDRO 1 1 NRR/DEST/ADE 8H 1 1 NRR/DEST/ADS 7E 1 0 NRR/DEST/CEB 8H 1 1 NRR/DEST/ESB 8D 1 1 NRR/DEST/ICSB 7 1 1 NRR/DEST/MEB 9H 1 1 NRR/DEST/MTB 9H 1 1 NRR/DEST/PSB 8D 1 1

.

NRR/DEST/RSB 8E 1 1 NRR/DEST/SGB 8D 1 1 NRR/DLPQ/HFB 10 1 1 NRR/DLPQ/QAB 10 1 1 NRR/DOEA/EAB 11 1 1 NRR/DREP/RAB 10 1 1 NRR/DREP/RPB 10 2 2 NRRJ3 /SIB 9A 1 1 NUDOCS-ABSTRACT 1 1 REG Fjj 02 1 1 RES/DSIR/EIB 1 1 RES/DSR/FRAB 1 1 RGN1 FILE 01 1 1 EXTERNAL: EGSG WILLIAMSFS 4 4 FORD BLDG HOYFA 1 1 H ST LOBBY WARD 1 1 LPDR 1 1 NRC PDR 1 ' NSIC MAYSFG 1 1 NSIC MURPHYFG.A 1 1 NOTES: 2 2 NOZE 'IO ALL 'RIDS" RICIPZEPIS:

PIZASE HELP US IO IlEDUCE %ASTl CGKPACT IHE DCjCUNEÃZ CGÃIK)L DESKF ROC'l-37 (EXT. 20079) %0 EIZKBRXS YOUR MHB HKH DISTBZBUTICN LIBTS FOR DOC(IMENIS YOU DQHFT NEED<

TOTAL NUMBER OF COPIES REQUIRED: LTTR 47 ENCL 46

NRC Form 388 U.S. NUCLEAR REGULATORY COMMISSION (9.83)

I( APPROVEO OMB NO. 31504104 LICENSEE EVENT REPORT ILER) EXPIRES: 8/31/88 F AC I LITY N A ME III DOCKET NUMBER (2) PAGE 3/

0 5 0 0 0 1 OF 0 TITLE (4)

Reactor Trip Due to Main Feedwater Regulating Valve Failure FVENT DATE (5) LER NUMBER (5) REPORT DATE I7) OTHER FACILI'TIFS INVOLVED (8)

SEGVENTIAL yh'. REVISION MONTH FACILITYNAMES DOCKET NUMBER(s)

MONTH OAY YEAR YEAR NVMSEA 'Ai NUMBER OAY YEAR 0 5 0 0 0 212 89 89 003 0 0 03 4 89 N/A 0 5 0 0 0 THIS REPORT IS SUBMITTED PURSUANT T0 THE REOUIREMENTS OF 10 CFR (I: /Check one or morc OI tnc IoliowrnP/ (11)

OPERATING POWE R

'0.402(bl MODE (SI 20.405(el(I i(i) 20A05(cl 50.35(cl(II 50.73(e) (2)(iv) 50.73( ~ )(2)(v) 73.71(b) 73.71Icl LEYEL (10) P 5 5 20.405(e l(1) (ii) 50.35 Ic I (2) 50,73( ~ ) (21(viil OTHER /Spetiry In AprrreCt

'rc 'yvynHX rg?e oe/ow enriin Tert, NIIC Form 5?'PNryr'Q?y r 20.405(e I) I I (ii)) 50 73(el(2) li) 50.73( ~ )(2)(wii)IAI 366AI 20.405( ~ l(l) I Iv) d0.73( ~ l(2)(i/I 50.73( ~ )12)(wii)IBI

"@. gp.

20.405( ~ l(1) (vl 50.73(e) (2 I (iii) 50.73( ~ )(2)(rrl LICENSEE CONTACT FOR THIS LER (12)

NAME TELEPHONE NUMBER AREA CODE Mr. Thomas P. Noonan, Plant Manager 41 264 3-1 25 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE OESCRIBEO IN THIS REPORT (13)

MANUFAC. REPORTABLE MANVFAC.

CAUSE SYSTEM COMPONENT p CAUSE SYSTEM COMPONENT TURER TVRER X JB FCV C63 5 Y

$ P:, ". '

SVPPLEMEN1'AL REPORT EXPECTFD (14) MONTH OAY YEAR EXPECTED SU 8 M I SS I 0N DATE (15I YES //I ycr, comp/etc EXPECTED SU84IISSIOIY DATE/

ABSTRACT ILimrt to /400 rpeccr. /c,, epprovimeteiy /i/teen r/nple torte tyPcwrinen /inn/ l(d)

On 2/12/89, with the Unit in Power Operation, a power reduction from 904 reactor power to 50% reactor power was in progress as part of End of Core Life programs. At 0048 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br />, operators noticed erratic operation of the "C" Main Feedwater Regulating Valve (MFRV). The operators placed the "C" MFRV in manual to control steam generator level. At 0108 hours0.00125 days <br />0.03 hours <br />1.785714e-4 weeks <br />4.1094e-5 months <br /> at approximately 55~ reactor power, the "A" Main Feedwater Pump was shutdown to reduce the pressure differential across the valve allowing easier valve movement and control. At 0120 hours0.00139 days <br />0.0333 hours <br />1.984127e-4 weeks <br />4.566e-5 months <br />, a turbine trip/reactor trip occurred due to a high water level in the "C" steam generator. The operators stabilized the plant in Hot Shutdown utilizing the Emergency Operating Procedures. The HC" MFRV was found to have sheared anti-rotation pins and the stem detached from the valve plug. The cause for the valve failure was attributed to hydraulic forces and vibration acting over time. The MFRVs were all disassembled, inspected and repaired as necessary. This event was reported to the Nuclear Regulatory Commission at 0300 hours0.00347 days <br />0.0833 hours <br />4.960317e-4 weeks <br />1.1415e-4 months <br />, in accordance with 10CFR50.72.b.2.ii.

There were no safety implications to the public as a result of this event. This type of event has previously been analyzed as stated in the Updated Final Safety Analysis Report, Section 15.1.2, "Feedwater System Malfunctions Causing an Increase In Feedwater Flow".

8903220424 8903i4 $)

NRC Form 358 PDR ADOCK 05000412 (9 83) S PNU

NRC Form 3SSA U.S. NUCLEAR RFOULATORY COMMISSION (943)

LICENSEE E ENT REPORT ILER) TEXT CONTINUATION APPROVED OMB NO. 3150-CI04 EXPIRES: 8/3)/88 FACILITY NAME <>co /r roqo/rod. o>> odd/I/orM/HRC Form36548l <<7)

DESCRIPTION On 2/12/89, with the Unit in Power Operation (Operating Mode 1),

Operations personnel were reducing reactor power from 90% to 50<

as part of End of Core Life programs. Prior to the Operating crew assuming the shift at 2300 hours0.0266 days <br />0.639 hours <br />0.0038 weeks <br />8.7515e-4 months <br /> on 2/11/89, the <<B<< Main Feedwater Regulating Valve (MFRV) had previously exhibited erratic valve control for steam generator water level. The <<B<<

MFRV was in the automatic mode, however, the valve was not controlling smoothly. At 0048 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br />, operators noticed erratic operation of the <<C<< MFRV. At 0108 hours0.00125 days <br />0.03 hours <br />1.785714e-4 weeks <br />4.1094e-5 months <br />, at approximately 554 power, the <<A<< Main Feedwater Pump was shutdown. At 0120 hours0.00139 days <br />0.0333 hours <br />1.984127e-4 weeks <br />4.566e-5 months <br />, the water level in the <<C<< steam generator increased to the high-high level setpoint (75%) causing. a turbine trip and feedwater isolation signal. The turbine trip caused a reactor trip, since reactor power was above the trip permissive of 49'.

The feedwater isolation signal caused the following actions to occur: 1) trip of the running main feedwater pump, 2) auto-start of the auxiliary feedwater pumps, and 3) closure of the main feedwater regulating valves and bypass valves.

Following the reactor trip, the operators utilized the Emergency Operating Procedures (E-0 "Reactor Trip or Safety Injection<< and ES-0.1 "Reactor Trip Response" ) to stabilize the plant in Hot Standby (Operating Mode 3).

APPARENT CAUSE OF THE EVENT The cause for this event was attributed to the failure of the

<<C<< Main. Feedwater Regulating Valve (2FHS*FCV498). This valve is a Copes-Vulcan, Model No. D-100-160, Part No. 16-FA37RG. The valve failure was attributed to the hydraulic forces and vibration, which over time, mechanically excite the valve, damaging the anti-rotation cage slots, plug guides, retaining pins and valve stem. The <<B<< Main Feedwater Regulating Valve was found to have damaged anti-rotation pins.

Nr)C FORM 300A 'U.S ~ CPCI )988-33<' )09 000)0 IS 83)

NRC Form 366A U.S. NUCLEAR REGULATORY COMMISSION 194)3)

LICENSEE ENT REPORT (LERI TEXT CONTINUA ON APPROVED OMB NO. 3160&)04 EXPIRES: 8/31/88 FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3)

YEAR SEQUENTIAL +"'2 REVISION NVM8ER ):. 1 NUMSSR spinto Beaver Valley Power Station, Unit 2 o s o o o 4 1 2 8 9 0 0 3 0 0 03oF 0 4 TEXT /lfmoro /4 rtr)o/rod, oto tddr)/ono/IVRC Form 3664'4/ OS)

CORRECTIVE ACTIONS The following corrective actions were taken as a result of this event:

Immediate:

1). Operations personnel utilized the Emergency Operating Procedures to stabilize the plant in Hot Standby.

2). The main feedwater regulating valves were disassembled and inspected. The anti-rotation pins were replaced on all main feedwater regulating valves.

Long-term:

An Engineering Memorandum has been generated requesting Engineering to identify an actuator and valve design which will eliminate the main feedwater regulating valve problems due to the hydraulic forces and vibration which over time, progressively damage the valves.

2). All three steam generators will be inspected during the First Refueling Outage for potent'ial loose objects.

SAFETY IMPLICATIONS There were no safety implications to the public as a result of this event. This type of event has previously been analyzed as stated in the Updated Final Safety Analysis Report (UFSAR),

Section 15.1.2, "Feedwater System Malfunctions Causing an Increase in Feedwater Flow". Additionally, all the required Engineered Safety Features (ESF) system components actuated as follows as a result of the steam generator high-high water level condition 1). Turbine trip, causing a reactor trip because reactor power was greater than the P-9 trip permissive, 2). Feedwater Isolation (FWI) signal, causing the following:

A). Trip of the running main feedwater pump, B). Automatic start of the auxiliary feedwater pumps 2FWE*P22, 23A and 23B),

C). Closure of the main feedwater regulating valves and bypass valves.

NRC FORM 34OA ~ V.S. CPOI )988-920-889 ~ OOOTO (94)3)

NRC Form 388A V.S. NUCLEAR REGULATORY COMMISSION (94)3)

LICENSEE ENT REPORT ILER) TEXT CONTINUA ON APPROVED OMB NO. 3)50&)04 EXPIRES: 8/31/88 FACILITY NAME (I) DOCKET NUMBER (2) LER NUMBER (8) PAGE (3)

SEOUENTIAL PP?r REvrsKIN YEAR gg NUMBER .Rrr. NUMBER 8eaver gal le Power Station, Unit 2 o s o o o 4 1 2 8 9 003 0 0 0 4 OF 0 4 TEXT IIImoro Z>>oo /4 re/rr/rod, Iroo EdcNane/HRC %%dmr 3684 9/ lll)

In addition, the Nuclear Steam System Supplier (NSSS) has evaluated the utility's engineering interpretation of the Steam Generator Parametric Loose Object Licensing Report (WCAP-12101),

which addressed the safety significance of the potential loose part (anti-rotation pin from 2FWS*FCV498) which could be trapped in the "C" steam generator tubesheet annulus. It was concluded that the estimated time required for the loose object to wear into a tube to the minimum allowable wall thickness, is 2.4 years. The NSSS concurred with this safety evaluation justifying continued operation of the remaining operating cycle.

REPORTABI LITY This event was reported to the Nuclear Regulatory Commission at 0300 hours in accordance with 10CFR50.72.b.2.ii. This written report is being provided in accordance with 10CFR50.73.a.2.iv, as an event involving a reactor protection system (RPS) or engineered safety fea'tures (ESF) system actuation.

PREVIOUS OCCURRENCES There have been no previous Licensee Event Reports issued on this type of event/equipment failure at Beaver Valley Power Station Unit 2.

NRC FORM 388A AU.S. GPOr IOSS SSB SSP I)0r)10 l94)3)

gled~

Duquesne Nuclear Group lt TelephOne (412) 393-6000 P,O, Box 4 Shippingporh PA 15077~

March 14, 1989 ND3SPM:0422 Beaver Valley Power Station, Unit No. 2 Docket No. 50-412, License No. NPF-73 LER 89-003-00 United States Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Gentlemen:

In accordance with Appendix A, Beaver Valley Technical Specifications, the following Licensee Event Report is submitted:

LER 89-003-00, 10 CFR 50.73 a.2.iv, "Reactor Trip Due to Main Feedwater Regulating Valve Failure".

Very truly yours, T. P. Noonan Plant Manager vhy Attachment

March 14, 1989 ND3SPM'0422 Page two CC: Mr. William T. Russell Regional Administrator United States Nuclear Regulatory Commission Region 1 475 Allendale Rd.

King of Prussia, PA 19406 C. A. Roteck, Ohio Edison Mr. Peter Tam, BVPS Licensing Project Manager United States Nuclear Regulatory Commission Washington, DC 20555 J. Beall, Nuclear Regulatory Commission, BVPS Senior Resident Inspector Mr. Alex Timme, CAPCO Nuclear Projects Coordinator Toledo Edison INPO Records Center Suite 1500 1100 Circle 75 Parkway Atlanta, GA 30339 G. E. Muckle, Factory Mutual Engineering, Pittsburgh Mr. J. N. Steinmetz, Operating Plant Projects Manager Mid Atlantic Area Westinghouse Electric Corporation Energy Systems Service Division Box 355 Pittsburgh, PA 15230 American Nuclear Insurers c/o Dottie Sherman, ANI Library The Exchange Suite 245 270 Farmington Avenue Farmington, CT 06032 Mr. Richard Janati Department of Environmental Resources P. O. Box 2063 16th Floor, Fulton Building

  • Harrisburg, PA 17120 Director, Safety Evaluation & Control Virginia Electric 6 Power Co.

P.O. Box 26666 One James River Plaza Richmond, VA 23261

,/