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See also: [[followed by::IR 05000528/1989050]]


=Text=
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{{#Wiki_filter:ACCELERATED
{{#Wiki_filter:ACCELERATED DISTIGBUTION DEMON>TINCTION SYSIEM r~t i  
DISTIGBUTION
 
DEMON>TINCTION
==SUBJECT:==
SYSIEM r~t i SUBJECT: Responds to NRC 900123 ltr re violations
Responds to NRC 900123 ltr re violations noted in Insp Rept 50-528/89-50.
noted in Insp Rept 50-528/89-50.
DISTRIBUTION CODE: IE01D COPIES RECEIVED:LTR ENCL SIZE: TITLE: General (50 Dkt)-Insp Rept/Notice of Violation Response NOTES ,S 05000528 REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)ESSION NBR 9003150098 DOC.DATE 90/02/21 NOTARIZED:
DISTRIBUTION
NO DOCKET N FACIL:STN-50-528 Palo Verde Nuclear Station, Unit 1, Arizona Publ'i 05000528., AUTH.NAME AUTHOR AFFILIATION CONWAY,W.F.
CODE: IE01D COPIES RECEIVED:LTR
Arizona Public Service Co.(formerly Arizona Nuclear Power RECIP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)R INTERNAL: RECIPIENT ID CODE/NAME PD5 PD ACRS AEOD/DEIIB DEDRO NRR/DLPQ/LPEB10 NRR/DREP/PEPB9D NRR/DRIS/DIR NRR/PMAS/ILRB12 OGC/HDS 1 RES MORISSEAU i D COPIES LTTR ENCL'.1 1 2 2 1 1 1, 1 1'1 1 1 1 1 1 1 1 1 1 RECIPIENT ID CODE/NAME PETERSON,S.
ENCL SIZE: TITLE: General (50 Dkt)-Insp Rept/Notice
AEOD AEOD/TPAD NRR SHANKMAN,S NRR/DOEA DIR 11 NRR/DREP/PRPB11 NRR/DST/DIR 8E2 NU QC-STRACT REG FI.'2 FILE 01 COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 2 2 1 1 1 1 1 1 1 1 EXTERNAL: LPDR NSIC NOTES 1 1 1 1 1 1 NRC PDR 1 1 D A b NOTE TO ALL"RIDS" RECIPIENTS:
of Violation Response NOTES ,S 05000528 REGULATORY
PLEASE HELP US TO REDUCE WASTE!CONTACT THE DOCUMENT CONTROL DESK, e ROOM Pl-37 (EXT.20079)TO ELMINATE YOUR NAME FROM DISIRIBUTION LISIS FOR DOCUMENTS YOU DON'T NEED!TOTAL NUMBER OF COPIES REQUIRED: LTTR26 ENCL 26 Arizona Public Service Company P.O.BOX 53999~PHOENIX.ARIZONA 85072-3999 WILLIAM F.CONWAY EXECUTIVE VICE PRESIDENT NUCLEAR 102-01606-MFC/TRB/JJN February 21, 1990 U.S.Nuclear Regulatory Commission Document Control Desk Washington, DC 20555  
INFORMATION
 
DISTRIBUTION
==Reference:==
SYSTEM (RIDS)ESSION NBR 9003150098
 
DOC.DATE 90/02/21 NOTARIZED:
Letter from R.Zimmerman, Director, Division of Reactor Safety and Projects, NRC to W.F.Conway, Executive Vice President Nuclear, Arizona Public Service, dated January 23, 1990  
NO DOCKET N FACIL:STN-50-528
 
Palo Verde Nuclear Station, Unit 1, Arizona Publ'i 05000528., AUTH.NAME AUTHOR AFFILIATION
==Dear Sirs:==
CONWAY,W.F.
Sub j ect: Palo Verde Nuclear Generating Station (PVNGS)Unit 1 Docket No.STN 50-528 (License No.NPF-41)Reply to Notices of Violation-50-528/89-50-01 and 528/89-50-02 File: 90-070-026 This letter is provided in response to the inspection conducted by Messrs.D.Coe, T.Polich, J.Ringwald, J.Sloan, W.Wagner, T.Meadows, and W.Ang.Based upon the results of the inspection, two (2)violations of NRC requirements were identified.
Arizona Public Service Co.(formerly Arizona Nuclear Power RECIP.NAME
The violations are discussed in Appendix A of the referenced letter.A restatement of the violations and PVNGS's responses are provided in Appendix A and Attachment 1 respectively, to this letter.The referenced letter noted that the violation involving failure to document completion of steps of a procedure is similar to previously identified violations and requires additional management attention.
RECIPIENT AFFILIATION
APS has taken additional actions since this occurrence to assure that personnel adhere to procedures.
Document Control Branch (Document Control Desk)R INTERNAL: RECIPIENT ID CODE/NAME PD5 PD ACRS AEOD/DEIIB
These actions are described in Attachment l.The refer'enced letter also noted that the events that occurred during the Unit 1 refueling operations demonstrated the need to improve communications between the various levels of APS management.
DEDRO NRR/DLPQ/LPEB10
In response to the event, a Human Performance Evaluation was conducted and the following corrective actions were implemented.
NRR/DREP/PEPB9D
The Unit 1 guideline"Communication of Unit 1 Status and Events" was revised to include additional guidance for potential refueling events which would require immediate notification of the Plant Manager or designee.The Unit 1 Plant Manager discussed this event and importance of prompt, accurate communication with the Unit 1 managers.f0Q 3I 50Qq g t'&P goOZP I~ooo gal PDg Document Control Desk Page 2 102-01606-WFC/TRB/J JN February 21, 1990 Should you have any questions regarding this response, please contact me.Very truly yours, WFC/TRB/JJN/kj Attachments CC: J.B.Martin D.H.Coe T.L.Chan E.E.Van Brunt A.C.Gehr J.R.Newman Document Control Desk Page 1 of 1 102-01606-WFC/TRB/3 JN February 21, 1990 APPENDIX A NOTICE OF VIOLATION Arizona Nuclear Power Project Palo Verde Unit 1 Docket Number 50-528 License Number NPF-41 During an NRC inspection conducted on November 13 through December 17, 1989, several violations of NRC requirements were identified.
NRR/DRIS/DIR
In accordance with the"General Statement of Policy and Procedure for NRC Enforcement Actions," 10 CFR Part 2, Appendix C (1989), the violations are listed below: Technical Specification 6.8.1 states, in part: "Written procedures shall be established, implemented and maintained covering...the recommendations in Appendix A'of Regulatory Guide 1.33, Revision 2, February 1978 Regulatory Guide 1.33, Revision 2, February 1978 recommends"Procedures for Performing Maintenance." Regulatory Guide 1.33, Revision 2, February 1978, is implemented in part by ANPP procedure 30DP-9MPOl, Revision 0, entitled"Conduct of Maintenance," Section 3.8, which states in step 3.8.6: "Work instruction steps, sections of steps and data sheets shall be properly documented at the time of performing the step or as soon thereafter if conditions do not permit." Contrary to the above, on November 14, 1989, Unit 1 Train"B" containment spray pump motor maintenance work order 362320 had progressed from Step 3.2.1 to Step 4.5 without corresponding documentation at the time of performing the step, under conditions which permitted such documentation.
NRR/PMAS/ILRB12
This is a Severity Level IV violation applicable to Unit 1 (Supplement I).B.10 CFR Part 50, Appendix B, Criterion V, states in part that activities affecting quality shall be prescribed by documented instructions, procedures, or drawings, of a type appropriate to the circumstances and shall be accomplished in accordance with these instructions, procedures, or drawings.Contrary to the above, on September 30, 1989, the licensee issued Special:Nuclear Material Transfer Set 1-3-1 to reload the Unit 1 reactor core, which was not appropriate to the circumstance in that it contained an error which directly resulted in partially inserting a fuel assembly in the core in other than its analyzed location.This is a Severity Level IV violation applicable to Unit 1 (Supplement I).l Document Control Desk Page 1 of 8 102-01606-WFC/TRB/J JN February 21, 1990 ATTACHMENT 1 Re 1 to Notice of Violation 50-528 89-50-01 A.I.REASON FOR VIOLATION On November 14, 1989, work to inspect motor terminal lugs on the Unit 1"B" train safety injection pumps.began in accordance with Work Orders 362318 and 36320.Since the work areas were potentially contaminated, working copies of the original work orders were made.After the assistant shift supervisor's approva1 was" obtained to start work, the original work orders were left in the electric shop and the electricians and a QC inspector proceeded to the work area with the working copies.Terminal lug inspection was in progress and almost complete on Work Order 362320 when the NRC inspectors observed that both the electrician and the QC inspector had not been signing off completed work instruction steps as the steps were performed on the working copy.The reason for the violation was cognitive error by the personnel involved.The electricians were interviewed following the event.Both electricians had thoroughly reviewed the work order preceding the actual work.The electricians were aware of the requirement to sign-off the steps in the work order while performing the work however, contrary to APS administrative requirements, the electricians periodically"checked-off" the steps on the working copy Document Control Desk Page.2 of 8 102-01606-WFC/TRB/J JN February 21, 1990 of the work order.The QC inspector was interviewed following the event.The QC inspector had completed the General Inspector Indoctrination Training, which included discussions of APS's requirement to sign-off steps as work was completed.
OGC/HDS 1 RES MORISSEAU i D COPIES LTTR ENCL'.1 1 2 2 1 1 1, 1 1'1 1 1 1 1 1 1 1 1 1 RECIPIENT ID CODE/NAME PETERSON,S.
However, the QC inspector had been on site for only three weeks and was unsure of the procedural'equirements to sign-off work steps as they are completed.
AEOD AEOD/TPAD NRR SHANKMAN,S
A.II CORRECTIVE STEPS TAKEN AND RESULTS ACHIEVED The NRC inspectors informed the responsible Work Group Supervisor about the violation of APS administrative requirements.
NRR/DOEA DIR 11 NRR/DREP/PRPB11
The Work Group, Supervisor immediately directed the electricians to stop work on Work Orders 362318 and 362320.Prior to continuing with the lug inspection, the work orders were amended to require a complete re-performance of the work.The work was re-performed and properly documented.
NRR/DST/DIR
No discrepancies were identified indicating improper performance of previous work.The steps in the amended work orders were properly signed-off as each step was completed.
8E2 NU QC-STRACT REG FI.'2 FILE 01 COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 2 2 1 1 1 1 1 1 1 1 EXTERNAL: LPDR NSIC NOTES 1 1 1 1 1 1 NRC PDR 1 1 D A b NOTE TO ALL"RIDS" RECIPIENTS:
No further discrepancies were identified during the performance of the work.
PLEASE HELP US TO REDUCE WASTE!CONTACT THE DOCUMENT CONTROL DESK, e ROOM Pl-37 (EXT.20079)TO ELMINATE YOUR NAME FROM DISIRIBUTION
Document Control Desk Page 3 of 8 102-01606-'WFC/TRB/JJN February 21, 1990 The individual electricians involved in the event were disciplined for not adhering to APS administrative control requirements (i.e., signing off on the work order as each step was complete).
LISIS FOR DOCUMENTS YOU DON'T NEED!TOTAL NUMBER OF COPIES REQUIRED: LTTR26 ENCL 26  
Additionally, maintenance personnel were briefed on the use of 30DP-9MPOl,"Conduct of Maintenance," which, in part, requires'roper documentation of completed steps at the time of performance.
Arizona Public Service Company P.O.BOX 53999~PHOENIX.ARIZONA 85072-3999
An effectiveness review of QC Inspector indoctrination training was performed immediately following the event.Interviews were conducted with other new QC Inspectors.
WILLIAM F.CONWAY EXECUTIVE VICE PRESIDENT NUCLEAR 102-01606-MFC/TRB/JJN
These inspectors stated that training adequately addressed the procedural requirement to document the completion of the work steps after the work step had been completed.
February 21, 1990 U.S.Nuclear Regulatory
An examination was administered to another group of new QC Inspectors regarding proper documentation of work and administrative controls for conduct of maintenance.
Commission
Based upon the test results, APS concluded that the requirements discussed above were adequately emphasized.
Document Control Desk Washington, DC 20555 Reference:
As a result of the training effectiveness review, APS concluded that training was adequate and the problem was an isolated occurrence limited to the QC Inspector.
Letter from R.Zimmerman, Director, Division of Reactor Safety and Projects, NRC to W.F.Conway, Executive Vice President Nuclear, Arizona Public Service, dated January 23, 1990 Dear Sirs: Sub j ect: Palo Verde Nuclear Generating
The QC inspector (contractor) was released from his duties with the PVNGS QC Department.
Station (PVNGS)Unit 1 Docket No.STN 50-528 (License No.NPF-41)Reply to Notices of Violation-50-528/89-50-01
Additionally, applicable indoctrination QC training was enhanced to include testing to validate effectiveness of the indoctrination training and the competence of the individual.
and 528/89-50-02
Document Control Desk Page 4 of 8 102-01606-WFC/TRB/J JN February 21, 1990 In addition to the corrective action's taken specifically in response to the event, APS has taken a number of steps to reemphasize to plant personnel the importance of strict adherence to procedures.
File: 90-070-026
A number of such steps are described in a letter to the NRC from J.N.Bailey, APS, dated November 17, 1989.A,III.CORRECTIVE STEPS THAT WILL BE TAKEN TO AVOID FURTHER VIOLATIONS APS believes the actions taken as described above are adequate to prevent recurrence.
This letter is provided in response to the inspection
A.IV.~~DATE WHEN FULL COMPLIANCE WILL BE ACHIEVED Full compliance was achieved on November 14, 1989, when Work Orders 362318&362320 were completed with the appropriate steps signed.
conducted by Messrs.D.Coe, T.Polich, J.Ringwald, J.Sloan, W.Wagner, T.Meadows, and W.Ang.Based upon the results of the inspection, two (2)violations
Document Control Desk Page 5 of,8*102-01606-WFC/TRB/J JN February 21, 1990 Re 1 to Notice of Violation 50-528 89-50-02 B.l.REASON FOR VIOLATION On September 29, 1989", PVNGS/APS Reactor Engineering personnel completed and approved the Material Balance Area (MBA)transfer sheet for movement of fuel and ultimately, the reload of the Unit 1 reactor core.The Reactor Engineering personnel reviewed the planned core loading pattern to determine the appropriate assembly for each location in the core, and entered the assembly designator on the MBA transfer sheet.They also identified the location of the assemblies on the Spent Fuel Pool (SFP)map and entered the SFP location designator on the MBA transfer sheet.During the preparation of the MBA transfer, sheet, the SFP location of one assembly was improperly transcribed.
of NRC requirements
Assembly PlD303 was stored in SFP location P28.However, during the preparation of the MBA transfer sheet for step 667, the SFP location of PID003 was entered as P38.The completed MBA transfer sheets were reviewed and approved by the responsible Reactor Engineer.However, the Reactor Engineer did not verify every entry on the MBA transfer sheets.The applicable procedure did not specifically require such detailed verification.
were identified.
Document Control Desk Page 6 of 8 102-01606-WFC/TRB/JJN February 21, 1990 B.II.CORRECTIVE STEPS TAKEN AND RESULTS ACHIEVED On November 16, 1989, while fuel loading was in progress, mimic boards of the SFP and reactor core in the control room were updated to reflect current assembly position.When the assembly from SFP location P38 (P1E004)was being inserted into the reactor core, reactor engineering personnel observed that the mimic placard on the mimic board represented a new fuel assembly and should have been located on the periphery of the core.Reactor engineering personnel immediately directed that the fuel movement be stopped.An immediate review of core loading pattern, the MBA transfer sheet, and the Spent Fuel Pool map was conducted.
The violations
The transcription error on the MBA transfer sheet was identified as the cause of this event.The MBA transfer sheets were revised to place assembly P1E004 into an intermediate location outside of the reactor core.Assembly PlD303 was retrieved from the SFP and inserted into the proper core location.Following discussions of the event, the cause and the additional procedural steps with the Operations.
are discussed in Appendix A of the referenced
letter.A restatement
of the violations
and PVNGS's responses are provided in Appendix A and Attachment
1 respectively, to this letter.The referenced
letter noted that the violation involving failure to document completion
of steps of a procedure is similar to previously
identified
violations
and requires additional
management
attention.
APS has taken additional
actions since this occurrence
to assure that personnel adhere to procedures.
These actions are described in Attachment
l.The refer'enced
letter also noted that the events that occurred during the Unit 1 refueling operations
demonstrated
the need to improve communications
between the various levels of APS management.
In response to the event, a Human Performance
Evaluation
was conducted and the following corrective
actions were implemented.
The Unit 1 guideline"Communication
of Unit 1 Status and Events" was revised to include additional
guidance for potential refueling events which would require immediate notification
of the Plant Manager or designee.The Unit 1 Plant Manager discussed this event and importance
of prompt, accurate communication
with the Unit 1 managers.f0Q 3I 50Qq g t'&P goOZP I~ooo gal PDg  
Document Control Desk Page 2 102-01606-WFC/TRB/J
JN February 21, 1990 Should you have any questions regarding this response, please contact me.Very truly yours, WFC/TRB/JJN/kj
Attachments
CC: J.B.Martin D.H.Coe T.L.Chan E.E.Van Brunt A.C.Gehr J.R.Newman  
Document Control Desk Page 1 of 1 102-01606-WFC/TRB/3
JN February 21, 1990 APPENDIX A NOTICE OF VIOLATION Arizona Nuclear Power Project Palo Verde Unit 1 Docket Number 50-528 License Number NPF-41 During an NRC inspection
conducted on November 13 through December 17, 1989, several violations
of NRC requirements
were identified.
In accordance
with the"General Statement of Policy and Procedure for NRC Enforcement
Actions," 10 CFR Part 2, Appendix C (1989), the violations
are listed below: Technical Specification
6.8.1 states, in part: "Written procedures
shall be established, implemented
and maintained
covering...the recommendations
in Appendix A'of Regulatory
Guide 1.33, Revision 2, February 1978 Regulatory
Guide 1.33, Revision 2, February 1978 recommends"Procedures
for Performing
Maintenance." Regulatory
Guide 1.33, Revision 2, February 1978, is implemented
in part by ANPP procedure 30DP-9MPOl, Revision 0, entitled"Conduct of Maintenance," Section 3.8, which states in step 3.8.6: "Work instruction
steps, sections of steps and data sheets shall be properly documented
at the time of performing
the step or as soon thereafter
if conditions
do not permit." Contrary to the above, on November 14, 1989, Unit 1 Train"B" containment
spray pump motor maintenance
work order 362320 had progressed
from Step 3.2.1 to Step 4.5 without corresponding
documentation
at the time of performing
the step, under conditions
which permitted such documentation.
This is a Severity Level IV violation applicable
to Unit 1 (Supplement
I).B.10 CFR Part 50, Appendix B, Criterion V, states in part that activities
affecting quality shall be prescribed
by documented
instructions, procedures, or drawings, of a type appropriate
to the circumstances
and shall be accomplished
in accordance
with these instructions, procedures, or drawings.Contrary to the above, on September 30, 1989, the licensee issued Special:Nuclear Material Transfer Set 1-3-1 to reload the Unit 1 reactor core, which was not appropriate
to the circumstance
in that it contained an error which directly resulted in partially inserting a fuel assembly in the core in other than its analyzed location.This is a Severity Level IV violation applicable
to Unit 1 (Supplement
I).l  
Document Control Desk Page 1 of 8 102-01606-WFC/TRB/J
JN February 21, 1990 ATTACHMENT
1 Re 1 to Notice of Violation 50-528 89-50-01 A.I.REASON FOR VIOLATION On November 14, 1989, work to inspect motor terminal lugs on the Unit 1"B" train safety injection pumps.began in accordance
with Work Orders 362318 and 36320.Since the work areas were potentially
contaminated, working copies of the original work orders were made.After the assistant shift supervisor's
approva1 was" obtained to start work, the original work orders were left in the electric shop and the electricians
and a QC inspector proceeded to the work area with the working copies.Terminal lug inspection
was in progress and almost complete on Work Order 362320 when the NRC inspectors
observed that both the electrician
and the QC inspector had not been signing off completed work instruction
steps as the steps were performed on the working copy.The reason for the violation was cognitive error by the personnel involved.The electricians
were interviewed
following the event.Both electricians
had thoroughly
reviewed the work order preceding the actual work.The electricians
were aware of the requirement
to sign-off the steps in the work order while performing
the work however, contrary to APS administrative
requirements, the electricians
periodically"checked-off" the steps on the working copy  
Document Control Desk Page.2 of 8 102-01606-WFC/TRB/J JN February 21, 1990 of the work order.The QC inspector was interviewed
following the event.The QC inspector had completed the General Inspector Indoctrination
Training, which included discussions
of APS's requirement
to sign-off steps as work was completed.
However, the QC inspector had been on site for only three weeks and was unsure of the procedural'equirements
to sign-off work steps as they are completed.
A.II CORRECTIVE
STEPS TAKEN AND RESULTS ACHIEVED The NRC inspectors
informed the responsible
Work Group Supervisor
about the violation of APS administrative
requirements.
The Work Group, Supervisor
immediately
directed the electricians
to stop work on Work Orders 362318 and 362320.Prior to continuing
with the lug inspection, the work orders were amended to require a complete re-performance
of the work.The work was re-performed
and properly documented.
No discrepancies
were identified
indicating
improper performance
of previous work.The steps in the amended work orders were properly signed-off
as each step was completed.
No further discrepancies
were identified
during the performance
of the work.  
Document Control Desk Page 3 of 8 102-01606-'WFC/TRB/JJN
February 21, 1990 The individual
electricians
involved in the event were disciplined
for not adhering to APS administrative
control requirements (i.e., signing off on the work order as each step was complete).
Additionally, maintenance
personnel were briefed on the use of 30DP-9MPOl,"Conduct of Maintenance," which, in part, requires'roper
documentation
of completed steps at the time of performance.
An effectiveness
review of QC Inspector indoctrination
training was performed immediately
following the event.Interviews
were conducted with other new QC Inspectors.
These inspectors
stated that training adequately
addressed the procedural
requirement
to document the completion
of the work steps after the work step had been completed.
An examination
was administered
to another group of new QC Inspectors
regarding proper documentation
of work and administrative
controls for conduct of maintenance.
Based upon the test results, APS concluded that the requirements
discussed above were adequately
emphasized.
As a result of the training effectiveness
review, APS concluded that training was adequate and the problem was an isolated occurrence
limited to the QC Inspector.
The QC inspector (contractor)
was released from his duties with the PVNGS QC Department.
Additionally, applicable
indoctrination
QC training was enhanced to include testing to validate effectiveness
of the indoctrination
training and the competence
of the individual.  
Document Control Desk Page 4 of 8 102-01606-WFC/TRB/J
JN February 21, 1990 In addition to the corrective
action's taken specifically
in response to the event, APS has taken a number of steps to reemphasize
to plant personnel the importance
of strict adherence to procedures.
A number of such steps are described in a letter to the NRC from J.N.Bailey, APS, dated November 17, 1989.A,III.CORRECTIVE
STEPS THAT WILL BE TAKEN TO AVOID FURTHER VIOLATIONS
APS believes the actions taken as described above are adequate to prevent recurrence.
A.IV.~~DATE WHEN FULL COMPLIANCE
WILL BE ACHIEVED Full compliance
was achieved on November 14, 1989, when Work Orders 362318&362320 were completed with the appropriate
steps signed.  
Document Control Desk Page 5 of,8*102-01606-WFC/TRB/J JN February 21, 1990 Re 1 to Notice of Violation 50-528 89-50-02 B.l.REASON FOR VIOLATION On September 29, 1989", PVNGS/APS Reactor Engineering
personnel completed and approved the Material Balance Area (MBA)transfer sheet for movement of fuel and ultimately, the reload of the Unit 1 reactor core.The Reactor Engineering
personnel reviewed the planned core loading pattern to determine the appropriate
assembly for each location in the core, and entered the assembly designator
on the MBA transfer sheet.They also identified
the location of the assemblies
on the Spent Fuel Pool (SFP)map and entered the SFP location designator
on the MBA transfer sheet.During the preparation
of the MBA transfer, sheet, the SFP location of one assembly was improperly
transcribed.
Assembly PlD303 was stored in SFP location P28.However, during the preparation
of the MBA transfer sheet for step 667, the SFP location of PID003 was entered as P38.The completed MBA transfer sheets were reviewed and approved by the responsible
Reactor Engineer.However, the Reactor Engineer did not verify every entry on the MBA transfer sheets.The applicable
procedure did not specifically
require such detailed verification.  
Document Control Desk Page 6 of 8 102-01606-WFC/TRB/JJN
February 21, 1990 B.II.CORRECTIVE
STEPS TAKEN AND RESULTS ACHIEVED On November 16, 1989, while fuel loading was in progress, mimic boards of the SFP and reactor core in the control room were updated to reflect current assembly position.When the assembly from SFP location P38 (P1E004)was being inserted into the reactor core, reactor engineering
personnel observed that the mimic placard on the mimic board represented
a new fuel assembly and should have been located on the periphery of the core.Reactor engineering
personnel immediately
directed that the fuel movement be stopped.An immediate review of core loading pattern, the MBA transfer sheet, and the Spent Fuel Pool map was conducted.
The transcription
error on the MBA transfer sheet was identified
as the cause of this event.The MBA transfer sheets were revised to place assembly P1E004 into an intermediate
location outside of the reactor core.Assembly PlD303 was retrieved from the SFP and inserted into the proper core location.Following discussions
of the event, the cause and the additional
procedural
steps with the Operations.
Shift Supervisor, fuel movement recommenced.
Shift Supervisor, fuel movement recommenced.
Subsequent
Subsequent to the event, on November 27, 1989, procedure 72AC-NF01"Control of SNM Transfer and Inventory" was revised to require independent verification of the MBA transfer sheets.This Document Control Desk Page 7 of 8 102-01606-WFC/TRB/JJN February 21, 1990 requirement was added to clarify that the existing requirement for approval included a 100 percent independent verification.
to the event, on November 27, 1989, procedure 72AC-NF01"Control of SNM Transfer and Inventory" was revised to require independent
To assess the potential safety significance if the fuel transfer error had not been detected promptly, an analysis was performed assuming that the fuel assembly had been completely inserted.The analysis demonstrated that adequate shutdown margin would have existed.Additionally, the PVNGS Updated Final Safety Analysis Report provides the analysis for the misloading of two assemblies in the event that the final fuel loading verification process did not identify a misloading of fuel assemblies.
verification
Therefore this event had no adverse effect on the health and safety of the public.The Unit 1 Plant Manager discussed this incident with the Unit 1 Managers to reemphasize management's intention that senior management be promptly advised of such occurences.
of the MBA transfer sheets.This  
B.III.CORRECTIVE STEPS THAT WILL BE TAKEN TO AVOID FURTHER VIOLATIONS APS believes the actions taken as described above are adequate to prevent recurrence.
Document Control Desk Page 7 of 8 102-01606-WFC/TRB/JJN
Document Control Desk Page 8 of 8 102-01606-WFC/TRB/JJN February 21, 1990 B.IV.DATE WHEN FULL COMPLIANCE WAS ACHIEVED Full compliance was achieved on November 16, 1989'hen the MBA transfer sheets were revised and the fuel assemblies were placed in the proper locations.}}
February 21, 1990 requirement
was added to clarify that the existing requirement
for approval included a 100 percent independent
verification.
To assess the potential safety significance
if the fuel transfer error had not been detected promptly, an analysis was performed assuming that the fuel assembly had been completely
inserted.The analysis demonstrated
that adequate shutdown margin would have existed.Additionally, the PVNGS Updated Final Safety Analysis Report provides the analysis for the misloading
of two assemblies
in the event that the final fuel loading verification
process did not identify a misloading
of fuel assemblies.
Therefore this event had no adverse effect on the health and safety of the public.The Unit 1 Plant Manager discussed this incident with the Unit 1 Managers to reemphasize
management's
intention that senior management
be promptly advised of such occurences.
B.III.CORRECTIVE
STEPS THAT WILL BE TAKEN TO AVOID FURTHER VIOLATIONS
APS believes the actions taken as described above are adequate to prevent recurrence.  
Document Control Desk Page 8 of 8 102-01606-WFC/TRB/JJN
February 21, 1990 B.IV.DATE WHEN FULL COMPLIANCE
WAS ACHIEVED Full compliance
was achieved on November 16, 1989'hen the MBA transfer sheets were revised and the fuel assemblies
were placed in the proper locations.
}}

Revision as of 09:54, 17 August 2019

Responds to NRC 900123 Ltr Re Violations Noted in Insp Rept 50-528/89-50.Corrective Actions:Work Orders Amended & Work Reperformed & Documented & Review of Core Loading Pattern, Mba Transfer Sheet & Spent Fuel Pool Map Conducted
ML17305A571
Person / Time
Site: Palo Verde Arizona Public Service icon.png
Issue date: 02/21/1990
From: Conway W
ARIZONA PUBLIC SERVICE CO. (FORMERLY ARIZONA NUCLEAR
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
102-01606-WFC-T, 102-1606-WFC-T, NUDOCS 9003150098
Download: ML17305A571 (12)


Text

ACCELERATED DISTIGBUTION DEMON>TINCTION SYSIEM r~t i

SUBJECT:

Responds to NRC 900123 ltr re violations noted in Insp Rept 50-528/89-50.

DISTRIBUTION CODE: IE01D COPIES RECEIVED:LTR ENCL SIZE: TITLE: General (50 Dkt)-Insp Rept/Notice of Violation Response NOTES ,S 05000528 REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)ESSION NBR 9003150098 DOC.DATE 90/02/21 NOTARIZED:

NO DOCKET N FACIL:STN-50-528 Palo Verde Nuclear Station, Unit 1, Arizona Publ'i 05000528., AUTH.NAME AUTHOR AFFILIATION CONWAY,W.F.

Arizona Public Service Co.(formerly Arizona Nuclear Power RECIP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)R INTERNAL: RECIPIENT ID CODE/NAME PD5 PD ACRS AEOD/DEIIB DEDRO NRR/DLPQ/LPEB10 NRR/DREP/PEPB9D NRR/DRIS/DIR NRR/PMAS/ILRB12 OGC/HDS 1 RES MORISSEAU i D COPIES LTTR ENCL'.1 1 2 2 1 1 1, 1 1'1 1 1 1 1 1 1 1 1 1 RECIPIENT ID CODE/NAME PETERSON,S.

AEOD AEOD/TPAD NRR SHANKMAN,S NRR/DOEA DIR 11 NRR/DREP/PRPB11 NRR/DST/DIR 8E2 NU QC-STRACT REG FI.'2 FILE 01 COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 2 2 1 1 1 1 1 1 1 1 EXTERNAL: LPDR NSIC NOTES 1 1 1 1 1 1 NRC PDR 1 1 D A b NOTE TO ALL"RIDS" RECIPIENTS:

PLEASE HELP US TO REDUCE WASTE!CONTACT THE DOCUMENT CONTROL DESK, e ROOM Pl-37 (EXT.20079)TO ELMINATE YOUR NAME FROM DISIRIBUTION LISIS FOR DOCUMENTS YOU DON'T NEED!TOTAL NUMBER OF COPIES REQUIRED: LTTR26 ENCL 26 Arizona Public Service Company P.O.BOX 53999~PHOENIX.ARIZONA 85072-3999 WILLIAM F.CONWAY EXECUTIVE VICE PRESIDENT NUCLEAR 102-01606-MFC/TRB/JJN February 21, 1990 U.S.Nuclear Regulatory Commission Document Control Desk Washington, DC 20555

Reference:

Letter from R.Zimmerman, Director, Division of Reactor Safety and Projects, NRC to W.F.Conway, Executive Vice President Nuclear, Arizona Public Service, dated January 23, 1990

Dear Sirs:

Sub j ect: Palo Verde Nuclear Generating Station (PVNGS)Unit 1 Docket No.STN 50-528 (License No.NPF-41)Reply to Notices of Violation-50-528/89-50-01 and 528/89-50-02 File: 90-070-026 This letter is provided in response to the inspection conducted by Messrs.D.Coe, T.Polich, J.Ringwald, J.Sloan, W.Wagner, T.Meadows, and W.Ang.Based upon the results of the inspection, two (2)violations of NRC requirements were identified.

The violations are discussed in Appendix A of the referenced letter.A restatement of the violations and PVNGS's responses are provided in Appendix A and Attachment 1 respectively, to this letter.The referenced letter noted that the violation involving failure to document completion of steps of a procedure is similar to previously identified violations and requires additional management attention.

APS has taken additional actions since this occurrence to assure that personnel adhere to procedures.

These actions are described in Attachment l.The refer'enced letter also noted that the events that occurred during the Unit 1 refueling operations demonstrated the need to improve communications between the various levels of APS management.

In response to the event, a Human Performance Evaluation was conducted and the following corrective actions were implemented.

The Unit 1 guideline"Communication of Unit 1 Status and Events" was revised to include additional guidance for potential refueling events which would require immediate notification of the Plant Manager or designee.The Unit 1 Plant Manager discussed this event and importance of prompt, accurate communication with the Unit 1 managers.f0Q 3I 50Qq g t'&P goOZP I~ooo gal PDg Document Control Desk Page 2 102-01606-WFC/TRB/J JN February 21, 1990 Should you have any questions regarding this response, please contact me.Very truly yours, WFC/TRB/JJN/kj Attachments CC: J.B.Martin D.H.Coe T.L.Chan E.E.Van Brunt A.C.Gehr J.R.Newman Document Control Desk Page 1 of 1 102-01606-WFC/TRB/3 JN February 21, 1990 APPENDIX A NOTICE OF VIOLATION Arizona Nuclear Power Project Palo Verde Unit 1 Docket Number 50-528 License Number NPF-41 During an NRC inspection conducted on November 13 through December 17, 1989, several violations of NRC requirements were identified.

In accordance with the"General Statement of Policy and Procedure for NRC Enforcement Actions," 10 CFR Part 2, Appendix C (1989), the violations are listed below: Technical Specification 6.8.1 states, in part: "Written procedures shall be established, implemented and maintained covering...the recommendations in Appendix A'of Regulatory Guide 1.33, Revision 2, February 1978 Regulatory Guide 1.33, Revision 2, February 1978 recommends"Procedures for Performing Maintenance." Regulatory Guide 1.33, Revision 2, February 1978, is implemented in part by ANPP procedure 30DP-9MPOl, Revision 0, entitled"Conduct of Maintenance," Section 3.8, which states in step 3.8.6: "Work instruction steps, sections of steps and data sheets shall be properly documented at the time of performing the step or as soon thereafter if conditions do not permit." Contrary to the above, on November 14, 1989, Unit 1 Train"B" containment spray pump motor maintenance work order 362320 had progressed from Step 3.2.1 to Step 4.5 without corresponding documentation at the time of performing the step, under conditions which permitted such documentation.

This is a Severity Level IV violation applicable to Unit 1 (Supplement I).B.10 CFR Part 50, Appendix B, Criterion V, states in part that activities affecting quality shall be prescribed by documented instructions, procedures, or drawings, of a type appropriate to the circumstances and shall be accomplished in accordance with these instructions, procedures, or drawings.Contrary to the above, on September 30, 1989, the licensee issued Special:Nuclear Material Transfer Set 1-3-1 to reload the Unit 1 reactor core, which was not appropriate to the circumstance in that it contained an error which directly resulted in partially inserting a fuel assembly in the core in other than its analyzed location.This is a Severity Level IV violation applicable to Unit 1 (Supplement I).l Document Control Desk Page 1 of 8 102-01606-WFC/TRB/J JN February 21, 1990 ATTACHMENT 1 Re 1 to Notice of Violation 50-528 89-50-01 A.I.REASON FOR VIOLATION On November 14, 1989, work to inspect motor terminal lugs on the Unit 1"B" train safety injection pumps.began in accordance with Work Orders 362318 and 36320.Since the work areas were potentially contaminated, working copies of the original work orders were made.After the assistant shift supervisor's approva1 was" obtained to start work, the original work orders were left in the electric shop and the electricians and a QC inspector proceeded to the work area with the working copies.Terminal lug inspection was in progress and almost complete on Work Order 362320 when the NRC inspectors observed that both the electrician and the QC inspector had not been signing off completed work instruction steps as the steps were performed on the working copy.The reason for the violation was cognitive error by the personnel involved.The electricians were interviewed following the event.Both electricians had thoroughly reviewed the work order preceding the actual work.The electricians were aware of the requirement to sign-off the steps in the work order while performing the work however, contrary to APS administrative requirements, the electricians periodically"checked-off" the steps on the working copy Document Control Desk Page.2 of 8 102-01606-WFC/TRB/J JN February 21, 1990 of the work order.The QC inspector was interviewed following the event.The QC inspector had completed the General Inspector Indoctrination Training, which included discussions of APS's requirement to sign-off steps as work was completed.

However, the QC inspector had been on site for only three weeks and was unsure of the procedural'equirements to sign-off work steps as they are completed.

A.II CORRECTIVE STEPS TAKEN AND RESULTS ACHIEVED The NRC inspectors informed the responsible Work Group Supervisor about the violation of APS administrative requirements.

The Work Group, Supervisor immediately directed the electricians to stop work on Work Orders 362318 and 362320.Prior to continuing with the lug inspection, the work orders were amended to require a complete re-performance of the work.The work was re-performed and properly documented.

No discrepancies were identified indicating improper performance of previous work.The steps in the amended work orders were properly signed-off as each step was completed.

No further discrepancies were identified during the performance of the work.

Document Control Desk Page 3 of 8 102-01606-'WFC/TRB/JJN February 21, 1990 The individual electricians involved in the event were disciplined for not adhering to APS administrative control requirements (i.e., signing off on the work order as each step was complete).

Additionally, maintenance personnel were briefed on the use of 30DP-9MPOl,"Conduct of Maintenance," which, in part, requires'roper documentation of completed steps at the time of performance.

An effectiveness review of QC Inspector indoctrination training was performed immediately following the event.Interviews were conducted with other new QC Inspectors.

These inspectors stated that training adequately addressed the procedural requirement to document the completion of the work steps after the work step had been completed.

An examination was administered to another group of new QC Inspectors regarding proper documentation of work and administrative controls for conduct of maintenance.

Based upon the test results, APS concluded that the requirements discussed above were adequately emphasized.

As a result of the training effectiveness review, APS concluded that training was adequate and the problem was an isolated occurrence limited to the QC Inspector.

The QC inspector (contractor) was released from his duties with the PVNGS QC Department.

Additionally, applicable indoctrination QC training was enhanced to include testing to validate effectiveness of the indoctrination training and the competence of the individual.

Document Control Desk Page 4 of 8 102-01606-WFC/TRB/J JN February 21, 1990 In addition to the corrective action's taken specifically in response to the event, APS has taken a number of steps to reemphasize to plant personnel the importance of strict adherence to procedures.

A number of such steps are described in a letter to the NRC from J.N.Bailey, APS, dated November 17, 1989.A,III.CORRECTIVE STEPS THAT WILL BE TAKEN TO AVOID FURTHER VIOLATIONS APS believes the actions taken as described above are adequate to prevent recurrence.

A.IV.~~DATE WHEN FULL COMPLIANCE WILL BE ACHIEVED Full compliance was achieved on November 14, 1989, when Work Orders 362318&362320 were completed with the appropriate steps signed.

Document Control Desk Page 5 of,8*102-01606-WFC/TRB/J JN February 21, 1990 Re 1 to Notice of Violation 50-528 89-50-02 B.l.REASON FOR VIOLATION On September 29, 1989", PVNGS/APS Reactor Engineering personnel completed and approved the Material Balance Area (MBA)transfer sheet for movement of fuel and ultimately, the reload of the Unit 1 reactor core.The Reactor Engineering personnel reviewed the planned core loading pattern to determine the appropriate assembly for each location in the core, and entered the assembly designator on the MBA transfer sheet.They also identified the location of the assemblies on the Spent Fuel Pool (SFP)map and entered the SFP location designator on the MBA transfer sheet.During the preparation of the MBA transfer, sheet, the SFP location of one assembly was improperly transcribed.

Assembly PlD303 was stored in SFP location P28.However, during the preparation of the MBA transfer sheet for step 667, the SFP location of PID003 was entered as P38.The completed MBA transfer sheets were reviewed and approved by the responsible Reactor Engineer.However, the Reactor Engineer did not verify every entry on the MBA transfer sheets.The applicable procedure did not specifically require such detailed verification.

Document Control Desk Page 6 of 8 102-01606-WFC/TRB/JJN February 21, 1990 B.II.CORRECTIVE STEPS TAKEN AND RESULTS ACHIEVED On November 16, 1989, while fuel loading was in progress, mimic boards of the SFP and reactor core in the control room were updated to reflect current assembly position.When the assembly from SFP location P38 (P1E004)was being inserted into the reactor core, reactor engineering personnel observed that the mimic placard on the mimic board represented a new fuel assembly and should have been located on the periphery of the core.Reactor engineering personnel immediately directed that the fuel movement be stopped.An immediate review of core loading pattern, the MBA transfer sheet, and the Spent Fuel Pool map was conducted.

The transcription error on the MBA transfer sheet was identified as the cause of this event.The MBA transfer sheets were revised to place assembly P1E004 into an intermediate location outside of the reactor core.Assembly PlD303 was retrieved from the SFP and inserted into the proper core location.Following discussions of the event, the cause and the additional procedural steps with the Operations.

Shift Supervisor, fuel movement recommenced.

Subsequent to the event, on November 27, 1989, procedure 72AC-NF01"Control of SNM Transfer and Inventory" was revised to require independent verification of the MBA transfer sheets.This Document Control Desk Page 7 of 8 102-01606-WFC/TRB/JJN February 21, 1990 requirement was added to clarify that the existing requirement for approval included a 100 percent independent verification.

To assess the potential safety significance if the fuel transfer error had not been detected promptly, an analysis was performed assuming that the fuel assembly had been completely inserted.The analysis demonstrated that adequate shutdown margin would have existed.Additionally, the PVNGS Updated Final Safety Analysis Report provides the analysis for the misloading of two assemblies in the event that the final fuel loading verification process did not identify a misloading of fuel assemblies.

Therefore this event had no adverse effect on the health and safety of the public.The Unit 1 Plant Manager discussed this incident with the Unit 1 Managers to reemphasize management's intention that senior management be promptly advised of such occurences.

B.III.CORRECTIVE STEPS THAT WILL BE TAKEN TO AVOID FURTHER VIOLATIONS APS believes the actions taken as described above are adequate to prevent recurrence.

Document Control Desk Page 8 of 8 102-01606-WFC/TRB/JJN February 21, 1990 B.IV.DATE WHEN FULL COMPLIANCE WAS ACHIEVED Full compliance was achieved on November 16, 1989'hen the MBA transfer sheets were revised and the fuel assemblies were placed in the proper locations.